ML20137C259
| ML20137C259 | |
| Person / Time | |
|---|---|
| Site: | Quad Cities |
| Issue date: | 12/31/1985 |
| From: | Boyd D NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
| To: | |
| Shared Package | |
| ML20137C216 | List: |
| References | |
| 50-254-85-27, 50-265-85-30, NUDOCS 8601160256 | |
| Download: ML20137C259 (18) | |
See also: IR 05000254/1985027
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U. S. NUCLEAR REGULATORY :COMISSION-
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REGION III
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Reports No. 50-254/85027(DRP); 50-265/030(DRP)
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Docket Nos. 50-254; 50-265
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Licensee:
Commonwealth Edison Company
Post Office Box 707
Chicago, IL 60690
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Fay.ility Name:
Quad Cities Nuclear Power Station, Units 1 and 2
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Inspection Conducted:
October 1 through December 7, 1985
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Inspectors:
A.L. Madison
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A.D. Morrongiello.
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N. A.
icholson,
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Reactor Projects Section 2D.
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Approved By:
D. C. Boyd, Ch' f ..
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. Date
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Inspection Summary:
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Inspection on October 1 through December 7, 1985 (Reports No. 50-254/85027(DRP);;
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50-265/85030(DRP))
Areas Inspected:
Routine, 6nannounced insp'ection by the resident inspectors
of actions on previous inspections findings; operations; radiological controls;
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maintenance / modifications; surveillance;housekesyt,ngprocedures; fire
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protection; emergency preparedness; security; quality assurance; quality
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control; administration; routine reports, LER review; bulletin followup;-
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regional requests; training; and independent inspection. The Jnspection
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. involved a total of 399 inspector-hours onsite by three NRC inspectors,
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including 79 inspector-hours onsite during off-shifts.
Results: Two violations were identified.
The first involved failure to
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' comply with technical specification requirements concerning fire detection
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equipment on the refuel floor.
T.he second involved inadequate review and
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corrective actions concerning a 10 CFR Part 21 report on Ruskin fire dampers.
Overall, the licensee's performance has improved in' operations and remained
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steady in all other areas.
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8601160256 860102
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ADOCM 05000254i
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DETAILS
1.
Persons Contacted
- N. Kalivianakis, Station Manager
- D. Bax, Production Superintendent
- T. Tamlyn, Technical Services Superintendent
T. Lihou, Technical Staff Supervisor
R. Roby, Assistant Superintendent Operations
- N. Griser, Senior Quality Assurance. Specialist
- B. Strub, Compliance Coordinator
The inspectors, through direct observation, discussions with licensee
personnel, and review of applicable records and logs, examined the areas
stated in the inspection summary and acccmplished the following inspection
modules.
37700
Design Changes and Modifications
42700
Plant Procedures
61726
Monthly Surveillance Observations
62703
Monthly Maintenance Observations
65051
Low Level Rad Waste Storage Facilities
71707
Operational Safety Verification
71710
ESF System Walkdown
90713
Review of Periodic and Special Reports
92700
Onsite Review of LERs
92702
Violation Followup
92703
IE Bulletin Followup'
92705
Followup - Regional Requests
92706
Independent Inspection
93702
Onsite followup of Events
2.
The inspectors verified that activities were accomplished in a timely
manner using approved procedures and drawings and were inspected / reviewed
as applicable; procedures, procedure revisions and routine reports were
in accordance with Technical Specifications, regulatory guides, and
industry codes or standards; approvals were obtained prior to initiating
any work; activities were accomplished by qualified personnel; the limiting
conditions for operation were met during normal operation and while
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components or systems were . removed from service; functional ~ testing and/
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or calibrations were performed prior to returning components or systems
to service; independent verification of equipment lineup and review of
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test results were' accomplished; quality control records and logs were
properly maintained and reviewed; parts, materials, and equipment were
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properly certified, calibrated, stored, and or maintained as applicable;
and adverse plant conditions including equipment malfunctions, potential
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fire hazards, radiological hazards, fluid leaks, excessive vibrations,
and personnel errors were addressed in a timely manner with sufficient
and. proper corrective actions and reviewed by appropriate management
personnel.
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Further, additional observations were made in,the following areas:
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Action 6n Fr'evious Inspection Findings ? >
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(1) '(Closed) Open Item'(254/84023-03; 265/84021-02(DRP)):
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Confirtsatory Action Letter Item,6. 761s item remained open
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pending the licensee's respotise/to ther report including the
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violation and long term corrective actions. Areas'of concern-
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were Shift Control-Room Engineer (SCRE) responsibilities and
authority and operators, remaining at the controls during
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off-normal events at the,other unit.
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The' licensee conducted extensive training and discussions with
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all SCREs and operators and updated their training program to
inc?ude lessons learned. -Also, the licensee revised applicable
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procedures to reflect the 'need for operators to remain at the
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cdntrols until' properly relieved and the' responsibilities of .
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the SCRE until relieved by the Shift Engineer. (SE) during
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f off-normal' events. . The inspectors._ reviewed the licensee's
actions, the revised procedures, and interviewed several
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operators and SCREs to determina adequacy.of long term
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corrective actions. The licens'ee's' actions were determined
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to be acceptable and no further concerns.were identified.
No
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further actions are required.
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(2) (Closed) Open Item'(254/85002-03 and 265/85002-03):
No
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procedure for independent verification to beiperformed on
release of equipment-from service.
This item was used to
track the implementation of procedures,that wodld address
independent verification of equipment ~' status when equipment
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was removed from service and when it was returned to service.
The licensee has changed the appropriate proceoures to~ address.
this item. The inspectors reviewed these changes and found
them adequate.
No further actions are required.
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(3) (Closed) Violation'(265/85007-01(DRP)): . Failure to Report
Scram While Shutdown.
On March 28,'1985, Unit two was. shutdown.
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for refueling.
A reactor scram signal from Main Steam Line
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High Radiat. ion was initiated by Radiograph ~ in the vicinity-of
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the detectors.o The licensee failed to report this-event as
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require'd by 10.CFR 50.72(G)(2)(ii) due to a misinterpretation
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of the requirement of a ." preplanned sequence of events."
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Discussion with the inspectors clarified the requirements and
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the licenseelrevised applicable procedures to ensure continued-
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compliance. 'No further~ actions are required.. -
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(4) '(0 pen) Unresolve'd Item'(254/850Df03; 265/85019-02(DRP)):-
Fuel Pool Radiation Monitor Trips'and Challenges to Standby
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. Gas Treatment.
The licensee has continued to investigate-
d this concern and additional spuric0s trips have ' occurred,
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providing. additional-opportunity to' isolate this; intermittent
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problem.
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One potential resolution was identified in Unit 2 LER 85-012,
Revision 01.
It was determined'that the practice of calibrating
the instruments in the' shop rather than in place was contributing
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to setpoint drift.. A procedure-change to QIS35-l',." Reactor
Building Fuel-' Pool Radiation Monitoring Calibration and
Functional Test Data Sheet".was submitted to eliminate this
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possible source.
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Also, the Instrument Maintenance Department has' discovered a
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higher than normal induced voltage on the IB Fuel Pool Monitor.-
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It is currently planned to reroute the signal cable for this
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monitor to avoid high' noise areas.
This reroute is_ expected
to-be completed by August 30, 1986.
Further testing will be
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-performed to determine the necessity of additional modifications.
No violations or deviations ~ were identified.
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Operations
As part of the licensee's ongoing efforts to improve station
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performance, a " quiet time"'from 2:15 p.m. to 3:15 p.m. has been
instituted in the control room.
This time period has been identified
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by past events as having a greater potential for confusion or
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miscommunication due to shift change and the increa' sed activity
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associated with that. The " quiet time" or restriction of activities
.._is expected'to reduce this. potential. Also, the station has' initiated-
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an afternoon planning meeting _ similar to_ the routine morning meetings
to help coordinate the afternoon and evening work activities.
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(1) Unit One
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On' November 11, 1985, while running the'1/2 Emergency Diesel
Generator (EDG) operability surveillance,-the output breaker.
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to Bus 13-1 would not close.
Since the surveillance was being
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run as required for "A" Low Pressure Coolant Injection (LPCI)
outage, an Unusual Ever.t was declared at-.2145.
The breaker was
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tested again (several times) and operated properly. The Unusual
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Event was terminated at 2150. .Further . investigation by the
licensee was inconclusive and no' reason for the apparent failure
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could be identified.
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On. November 24, 1985~at 1725, the 1/2 EDG was again deciared
inoperable when' it failed 'to ~ close~ 'on- Bus 113-1.
Since the'ID
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Residual Heat Removal-(RHR) Service Water pump was also out of'
, service, an Unusual! Event was declarediand the Unit. began to._
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shut down.' The AssistantlSuperintendent for: Maintenance,Lthe;
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Master Electrician,. Electrical' Engineers from Operational-'
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-Analysis Department (OAD) and: Technical-Support worked
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'throughout the night and determined that the'HACR-1' relay-(this;.
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~ prevents closing the outputtbreaker when not electrically -
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. synchronized and is not'used during; emergency actuation) had-
ipoorly crimped. wires which may produce poor: electrical-
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connection and resulted in this intermittent problem.
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wires were recrimped and the breaker tested satisfactorily.
Following a two hour operability run, the 1/2 EDG was declared
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operable at 0850 on November 25 and the Unusual Event was
terminated.
The HACR-1 relay wire crimping problem had been previously
identified by the licensee as potentially generic to
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Commonwealth Edison (CECO) only.
These relays are
manufactured by Commonwealth Edison for use at all their
facilities.
Since the relay is not electrically in use
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during emergency actuation of the EDG, it is not considered
safety related and thus no 10 CFR Part 21 report was issued.
However, a notice was issued to all CECO facilities which
required 0AD to check and verify adequate crimping on all
similar relays.
Apparently, this was not accomplished at
Quad Cities.
Subsequent to the November 24, 1985 event, the
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licensee verified adequate crimping on all EDGs at Quad Cities
Station.
Pending determination of the reason _why these relays
were not checked, this item will be tracked as an Unresolved
Item (254/85027-01; 265/85030-01(DRP).
Following the termination of the Unusual Event, the licensee
continued to investigate the 1/2 EUG to verify that the
intermittent problem had been resolved.
Additional problems
were encountered and at 1025 on November 25, an Unusual Event
was again declared. Since'it appeared that the 1/2 EDG was
never operable, the start time of the Unusual Event was
conservatively set at.1725 on November 24.
Thus, with power
reduced to 100 MWE, Unit One was scrammed at 1230 in order to
comply with the Limiting Condition of Operation which required
cold shutdown in 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
It was determined that the problem was an intermittent fault in
the " fully racked in switch" on the diesel out'put breaker.
Following repairs to the 1/2 EDG output breaker and thorough
testing, the Unit was returned to operation on November 26, 1985.
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Unit Two
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On October 3, 1985, while at full power, it was discovered at'
approximately 1840 that the 28_RHR and 28 Core Spray (CS) room-
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cooler. fan belts were broken. At 1900 an Unusual Event was
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declared and a controlled' shutdown wa's~ initiated.- The belts
were replaced, the room coolers were tested operable,- and the
Unusual Event was terminated at 2210.
At 0510 on October 10, 1985, Unit 2 EDG output breaker tripped
during routine surveillance. 'The breaker was reset and tripped
again at 0518.
This time indicating a ground on control power.
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Concurrently, the containment cooling valves for RHR were out of
service for Environmental Qualification (E.Q.) modifications;
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therefore, at 0536~an Unusual Event was declared.
The-valves
were immediately returned to service and the Unusual Event was
secured at 0537.
The problems with the EDG were then
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investigated and repaired.
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At 2246'on October 15, 1985, Unit 2 experienced a reactor scram ~
from 100% power. While performing routine. surveillance,Lan
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instrument mechanic committed an' inadvertent valving error on-a
Yarway. .This caused a pressure transient on the entire instrument-
rack which in turn caused a low low level scram and a Group I,.
II, and III isolation.
All systems functioned as expected.
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licensee lected to proceed to cold shutdown and perform E.Q.
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modifications in the drywell as well as repairs to the Reactor :
Water Cleanup pumps and Reactor' Building Equipment Drain pumps
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and preventive maintenance to the unit output transformer. 'The-
Unit returned to service on October 24, 1985.
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On November 7, 1985, the inner seal for'the~28 recirculation
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pump failed.
The licensee' decided to place'. Unit 2 in cold
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shutdown and to effect repairs rather than rely on the outer-
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seal for an extended period.
The unit was returned to service
on November 9.
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During plant tours of Units 1 and 2, the inspectors walked down
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the accessible portions of the High Pressure Coolant Injection
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Systems, the Residual Heat Removal systems, and the Core Spray
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Systems and performed the applicable portions of Inspection <
Procedures 71710 "ESF System Walkdown".
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No violations or deviations were identified.
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Radiological Controls
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(1) The radiation protection department received information about.
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a situation at the Cooper Nuclear. Station.
At that station dose
rate levels between the~ reactor and the fuel pool at an elevation
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corresponding to the. head-flange area were approximately 280R/hr.
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The resident inspector accompanied a health physics' technician
to investigate whether or.not a.similar condition existed at
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Quad Cities. -The survey revealed'that the situation does not-
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exist at this site.
(2) The licensee-is building.an onsite Interim R'dwaste Storage
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Facility (IRSF) for low level radwaste storage in anticipation.
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of the closure of the burial sites on January.1,- 1986, authorized
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by 1980 Congressional legislation. An inspector reviewed the-
blueprints and toured the IRSF. :The IRSF .is a generic CECO
design,'similar to those under construction at the Zion'and
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LaSalle stations, and is located within the protected area for
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access and radiological controls.
Processed containers, meeting.
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DOT and NRC shipping limits will be transferred from the radwaste'
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processing area to the IRSF by truck. .As an ALARA meosure, the;
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-containers will.be positioned in the IRSF storage vault by;
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remotely operated crane; no personnel' access to the vaults' has -
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been designed.
Licensee representatives estimate storage capacity
at approximately four years with low level processed resin being
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the primary component.
No dry active waste.will be stored in
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the IRSF; other alternatives. are being evaluated.
Projected
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completion date for the IRSF is January 2,'1986.
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The IRSF is a poured concrete-structure building in accordance
with the Uniform Building Code.
In accordance with current NRC-
guidance for onsite low level storage facilities the111censee
has conducted a 10 CFR 50.59 evaluation of safety issues
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associated with the IRSF.
This evaluation, pending' final
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approval, was reviewed by an inspector. The evaluation will be
further reviewed pending additional generic guidance from NRC'
rad waste staff. This review will be tracked as an Open Item
(254/85027-02,~265/85030-02(DRSS)).
The licensee is currently developing operational and radiological
surveillance programs for the IRSF.
In response to the
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inspector's comments, the licensee agreed to:
(1) establish a.
monitoring program for airborne activity, waterborne activity,
and general radiation fields in the IRSF (0 pen Item:(254/85027-03;
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265/85030-03)); (2) evaluate the possibility of hydrogen and.
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gaseous generation from spent resins, and determine the-need for-
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monitoring (0 pen Item (254/85027-04;'265/85030-04)); (3) establish
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an inspection program of container integrity on a routine basis
(0 pen Item (254/85027-05;- 265-85030,-05));- and.._(4) evaluate the -
use of grating positioned directly on-the-concrete floor to
minimize condensate accumulation on contair ers (0 pen Item
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(254/85027-06; 265/85030-06)).
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Maintenance
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The following activities were observed / reviewed:
(1) Observed repacking of Olit 1 drywell sample pump.
(2) Observed installation of Unit 2. Instrument Air Compressor heat-
exchanger.
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(3) Observed installation of temperature control-valves on Unit'~1
and 2 Reactor Building Closed Cooling Water System (RBCCW).
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-(4) Observed replacement of the Unitil~and 2 Instrument Air
Compressor Motor.
(5) Observed removal-of Unit 2 RBCCW-pump motor for-bearing
replacement.
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-(6)- Observed trouble shooting of Unit ~2 Scram Discherge. Volume-
level, alarms.
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(7) Observed testing of various valves following E.Q. modifications
for Unit I and 2.
(8) Reviewed E.Q. modifications of drywell components for Unit 1
and 2.
(9) Reviewed corrective maintenance on 1/2 EDG.
Via Generic Letter 85-15, " Equipment Qualification", the Commission
promulgated a deadline of midnight, November 30, 1985 for the
completion of all modifications to comply with Environmental
Qualification concerns. Throughout the year, the licensee has
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diligently worked to comply with this requirement and has taken
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several small outages for this purpose as well as extending planned
and unplanned outages.
Aggressive management attention combined
with good planning and the cooperative attitude of the maintenance
staff resulted in the completion of all modifications on November 29,
1985.
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The inspectors have noted an improvement in interstation communication
with the CECO organization as evidenced by problems with E.Q. wiring
of Limitorque valve motors at Zion station being immediately
communicated to Quad Cities for resolution.
Also, problems at Quad
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Cities station are transmitted to other CECO stations through several
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formal and informal communication channels.
However, one recent event
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at LaSalle County station was not' communicated to Quad Cities although
the problem may have been applicable.
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LaSalle station experienced a problem with Mobil Vaprotec light oil
used in their Reactor Core Isolation Cooling turbines and switched
to Gulf Crest 32 with a special additive. While Quad Cities uses
Mobil Vaprotec light oil in RCIC and High Pressure Coolant Injection
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(HPCI) turbines, this information was not comniunicated by LaSalle
station. Quad Cities has not experienced a problem in the past with
this oil, but, when informed by the resideat inspectors of this
potential, the maintenance staff did commit to investigate the issue
further.
Resolution of this concern will be tracked as an Open Item
(254/85027-07; 265/85030-07).
No problems ~have been identified to
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date however, this is evidence that further improvements in
Corporate communication channels are required'to ensure that-
experiences at other stations are incorporated into the
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activities of Quad Cities.
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No violations or deviations were identified.
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Surveillance
The following activities were observed / reviewed:
(1) Observed performance in the field of high reactor pressure
scram surveillance for Unit 2.
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(2) Observed control. room portions of pump and valve operability
check for RHR on linit 2.
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(3) Observed performance in the field of low low level scram
testing for Unit 1.
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(4) Observed control roo,a portions of operability testing of
the 1/2 EDG.
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(5) Observed control room portions of pump and valve functional
testing for Unit 2 core spray.
(6) Observed tip traces for Unit 2 and subsequent APRM adjustments.
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Procedures Reviewed
QAP 500-15
Conduct of Maintenance
Revision 1
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QAP 500-13
Environment Qualification Program
Revision 2
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-QAP 300~5
Shift Change for Shift Control
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Room Engineer / Shift Technical' Advisor Revision-5
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QAP 300-7
Shift Change for Nuclear Station
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Revision 7 -
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QAP 900-S2
New Control Rod. Receiving Inspection
. Revision 3
QMP-100-3
Fire Prevention for Welding and
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Cutting =
Revision 5-
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QMP 100-S1
Welding and Cutting Permit-
Revision 3
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Q0P 1100-1
Standby Operation'of Standby Liquid
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Re'ision 4
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Control System
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QOP 1100-2
Injection of Standby Liquid Control
Revision 4
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QAP 300-2
' Conduct of Shift Operations
- Revision 16
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Review of Routine and Special Reports-
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The inspectors reviewed the monthly performance reports for Units-1:
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-and 2 for the months of September and October.-
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No violations.or deviations were identified.
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LER Review
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.(1) (Closed) LER 85-016; Revision 00: ~ Refuel floor monitor spike
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and start of standby gas treatmeht.,
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On September 5, 1985, Unit 1 was in the RUN mode at approximately
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100 percent of !sted core thermal power.
At 1348 hours0.0156 days <br />0.374 hours <br />0.00223 weeks <br />5.12914e-4 months <br /> the
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Control Room received a spurious high alarm and trip of the IB
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Fuel Pool Radiation Monitor.
The Reactor Building Ventilation
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isolated and the Standby Gas Treatment initiated.
No abnormal
'!
radiation levels were. discovered and these systems were manually-
reset at 1350 hours0.0156 days <br />0.375 hours <br />0.00223 weeks <br />5.13675e-4 months <br />.
The cause of this trip was probably.
electrical noise interference.
The Instrument Maintenance
Department has discovered a' higher than norma 1' induced voltage
on the IB Fuel Pool Monitor. 'It is currently planned to reroute
the signal cable for this monitor to avoid high noise areas.
This reroute is expected to be completed by August 30, 1986.
The' ongoing problems with Fuel Pool Radiation Monitors has been
addressed in previous ~ LERs and . Inspection: Reports.
This LER.is
considered closed, however, the~overall concern and ultimate
resolution is being tracked by Unresolved Item (254/85017-03;.
265/85019-02(DRP)).
(2) (Closed).LER 85-017,.Revisio'n 00: ' Reactor Core Isolation Cooling
Discharge Valve would not open.
On October 15, 1985, Unit One was in the RUN mode at 90 percent
of rated core thermal-power.
During the performance of-
surveillance QOS 1300-3, " Reactor Core Isolation Cooling Motor
Operated Valve Operability Test", it was discovered that the RCIC
pump. discharge valve would not open from the Control Room after
it was closed.
RCIC was, therefore, declared inoperable.
It
was found that the main contactor in the breaker for the motor-
operator for the valve was dirty and would not close completely,
thereby failing to supply power to the motor.
After the breaker-
was reset, the valve was successfully cycled three times and
The buildup of dirt on the main'cantactor was the result of
using the lubricant on the main contactor's pivot point. The
lubricant collects dirt which= increases the; viscosity of the
mixture to a value that prevents the main breaker from working:
properly.' The use of this lubricant was a recent change to the
surveillance procedure and had not been:used on other breakers.
-This practice has been discontinued as a result-of this event.
No further actions are required.
Unit 2
'(1) -(Closed) LER 84-013 Revision 00:
Missed Service Water Grab
Samples. This. item remained open pending revisions to the
sampling and administrative review procedures to ensure
>
continued comp 1iance. eAdequate revisions were implemented and
reviewed by-the inspectors.- No further actions are required.
'9-
.
. . .
.. - .- . . - .
.
.
-.
.
.
.- - -.
-
.
.
.
!~
'
4:
(2) '(Closed) LER 85-012, Revision 00 and 01: On December 1, 1984,
3
' Unit 2 was operating'at approximately 99 percent core thermal
,
'
power.
At 9:25 a.m., the Reactor Building Fuel Pool Channel iB'
Area Radiation Monitor ~ tripped, isolating the Reactor Building
Ventilation and starting the. Standby Gas Treatment System.
A-
' '
- .
check on both channels of the Fuel Pool' Area Radiation Monitors
1
i.
did not indicate any abnormal radiation levels. The Reactor
Building Ventilation and Standby Gas Treatment were returned.
to normal.
The Instrument Maintenance Department found that-the
trip setpoint of the iB' Radiation Monitor-was at 35 mr/ hour
rather than the normal'setpoint'of 100 mr/ hour, allowing normal.
t
,
instrument noise to trip the monitor. Corrective action was to
recalibrate and functionally test the monitor.
The cause of-the
setpoint being set at 35 mr/ hour w'as'dtfe to the instrument being
I
calibrated in the Instrument Maintenance shop rather than-in
place. The variations in using two different power supplies and
j
physical movement contributed to the set ~ point drift.
i
A search through two previous sets of calibration data for this
specific instrument revealed that its' calibration"setpoint had
'
drifted abnormally during'the last several months. A procedure
c.hange to QIS 35-1, " Reactor Building Fuel Pool Radiation
i
Monitoring Cal.ibration and Functional. Test Data Sheet" was
submitted to have the Trip Unit calibrated in place, using the~
.
normal power supply.
The ongoing problems with Fuel Pool Radiation Monitors has been-
addressed in previous LERs and Inspection reports. _This'LER is
'
!
considered closed, however, the overall concern and ultimate
F
resolution is being tracked as Unresolved Item (234/85017-03;
i
265/85019-02(DRP)).
l
(3) (0 pen) LER 85-018, Revision 00:
Low Condenser Vacuum Set Point
Drift.
!
~
On August 26, 1985, at 11:55 a.m., Unit 2 was operating-in the
g
RUN mode at approximately 98-percent core thermal power. ~During.
.
the performance of " Low Condenser Vacuum Calibration",'QIS 19-1,
1
i
the setpoints'of. Pressure Switches PS-2-503A and PS-2-503C were
found to have drifted to 20 8 inches Hg vacuus:and 19.4 inches
'
Hg vacuum, respectively.
- he switches were recalibrated'to
j
within Technical Specifications.
.
I
.
There have been 13 previous occurrences of-~setpoint driftEfor-
,
this type of switch. -Therefore, the licensee is investigating-
enginee*ing solutions-or possible replacement of these switches,
-
with more stable switches.~ ~Pending final resolution, this LER
i
will' remain open.
'
i.
.. Main Steam'Is'olation Valve
1
l
(4) _(Closed) LER 85-019, Revision 00:
. .
.
.
.
p
Closure Times and Initiation of Orderly Shutdown.
-i
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2
- On September 8, 1985, Unit 2 was operating at 72 percent of
'
rated core thermal power.
At'0225 hours0.0026 days <br />0.0625 hours <br />3.720238e-4 weeks <br />8.56125e-5 months <br />, while performing Main
Steam Isolation Valve Closure Time Testing (QOS 250-4), valves
'
A0 2-203-1B,:2-203-1C, and 2-203-10 had closure times of 2.72
'
. seconds, 2.89 seconds, and 2.80 seconds, resputively. Table
,
4-
3.7.1, of the Technical Specifications, requires a closing time:
!
of 3 to 5: seconds. At 0820 hours0.00949 days <br />0.228 hours <br />0.00136 weeks <br />3.1201e-4 months <br /> a Unit 2 Reactor shutdown
commenced per Technical Specification 3.7.D.3.
A Drywell. entry
was made to adjust to the closure times; the three valves were
s
retested satisfactorily and the Reactor shutdown was terminated
4
at 300 MWe, at 1314 hours0.0152 days <br />0.365 hours <br />0.00217 weeks <br />4.99977e-4 months <br />.
i
The cause was the speed control valve adjustment on the
hydraulic control cylinder drifting aut of adjustment.
There'
have only been four previous occurrences of'a similar nature
.
during the lifetime of_ Unit 2, therefore no further corrective
.
,
action is planned or required at this time.
j
F
(5) (Closed) LER 85-020, Revision 00:
Unit 2 Condenser 5 foot
,
!
Circulating Water Pump Trips Out of Service.
'
!
{
On August 26, 1985, Unit 2 was operating ~at 97 percent of rated
core thermal power.
The Equipment Operator was performing QOS'
,
i
030-3, " Condenser Pit High Level and 5 Foot Trip Circuitry
'
Test".
The test is performed by putting a pencil =into the'
opening of the level switch chamber and actuating the level
switch. While the test is being performed, the circulating-
water pump high level trip test- switches are open to disabia the
circulating water pump trips. -During the-test,.the pencil that
was used to actuate the switch broke off inside the 3 foot
.
.
level alarm switch.
A work request was then written for the .-
l
Electrical Maintenance Department to remove;the_ broken pencil.in
'
the level alarm switch.
!
On September 16, 1985, an~ Electrician reported to the Shift
'
Engineer for permission to work on the~1evel alarm switch. The
<
!
Shift Overview Superintendent.(SOS), observing their discussion,
!
suggested that they disable the trips while' removing the pencil
so that the electrician would'not accidentally trip the circulating
'
,
- -
water pumps.
The Shift Foreman suggested if they were_ going to
i
disable the trips, they should take them out of. service for the
Shift Engineer so they would not forget to-return them to service.
!
I
The Shift Control Room Engineer (SCRE) completed the out of
service process and all,four-pump trips were taken out of
service.
This action,- however, did not affect the operability-
,
- of the 3 foot alarm switches.because their circuitry.is
i
physically separated from that of the.5 foot pump trips. The
'
Electrician was.given permission'to go~to work at:1345. hours.on
l
September 16, 1985, and the job was completed at 1415-hours on
L
the same. day.
He then informed the Unit 2.0peratorr.that the
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job was completed, but the pump trips were not. returned to
service until 0730 hours0.00845 days <br />0.203 hours <br />0.00121 weeks <br />2.77765e-4 months <br />'on September'17, 1985, when the
situation was identified by the licensee during normal
supervisory reviews.
.
t-
Technical Specification 3.5.H.2 requires the condenser pit..
water level switches to trip the condenser circulating water
i
i
pumps and alarm in the Control Room-.if the water level in the
condenser pit exceeds a level of.5 feet above the pit floor.
If a failure occurs in one of these trip and alarm circuits,
the_ failed circuit is required to be immediately placed in a
j
trip condition.
Reactor operation is permissible for the-
following seven days'unless the circuit is sooner made. operable,
or an orderly shutdown must be initiated and the Reactor.must
'
be-in a Cold Shutdown condition within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
>
The switches were taken out of service, and the pump trips were
disabled. More than one switch was taken out of service but
they were not placed in a trip condition, and a seven day clock
,
was not started contrary to Technical Specification 3.5.h.2.
'
!
L
The cause of this deviation is that the Shift Foreman, Shift
'
Engineer and Shift Overview Supervisor involved in the initial
l
discussion were more concerned with preventing an inadvertent
'
circulating water pump trip and did not consider the Technical'
!
Specification requirements.
The fact that the testing procedure
' '
required that the trips be disabled while the Equipment Operator
,
is under the hotwell was a contributing factor in the decision
j
to disable the pump trips.
!
i
The people involved in the decision'were not familiar with the .
circuitry of the pump trips. The 3. foot alarm switch is physically
separated from the 5 foot pump' trips.
Therefore, it was'not
!
necessary to remove the 5 foot pump trips to work on the 3_ foot
i
level alarm switches. There.are four pump trip switches, of-
1
which two are needed to energize the pump trip relays.
-
The SOS stated that he never meant for the Shift Engineer to
.
l
- disable all of the pump' trips.
If:he had been familiar with the
i
electrical prints, he would have known that the knife. switches-
'
'
are-in the trip logic from the relay's energized contacts and
,
not in the level switch circuit.
!'
The.only person not directly involved in the initial decision-
who~ could have provided an independent check of the out-of-service.
'
4 -
decision was_the day shift SCRE.
However,'he failed to check the-
?
I
Technical Specifications for violations.
~
j
. The 1500-2300 Shift Engineer was not made' aware during the. shift
'
i
. change with the 0700-1500 Shift Engineer that all of the trip.
circuits were disabled.
Consequently, the 2300-0700 Shift-
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Engineer _was also not aware of the circulating pump trip out ofL
1.
service.
This was the contributing cause of~not having the_ pump
'i
!
trips returned to service'in a timely manner.
A meeting was held with the Production Superintendent,-Assistant
Superintendent of Operations,- Operating Engineers, Shift
Engineers, Shift Control. Room Engineers, and Shift Foremen to--
discuss this' specific' event in detail and this information was
included in operator training and retraining lessons.
[
Several past errors have happened at shift changes when there is
!
increased activity. This activity _is mainly.from maintenance,
,
either returning the day's work to service or requesting.
l
equipment out of service fur the'next day.
Several steps were
j
taken to reduce this activity.
4
.
'Ar. afternoon meeting was initiated at 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br /> between the
!
maintenance schedulers and the Operating Engineers. ' Equipment'
l-
returned to service and requests for the next-day's'out of
service take place in thir. meeting.-
,
Station personnel have.been directed not to disturb,.the
Operating personnel involved in a shif; .hangc during the
period from 1415 hours0.0164 days <br />0.393 hours <br />0.00234 weeks <br />5.384075e-4 months <br /> to 1515 hours0.0175 days <br />0.421 hours <br />0.0025 weeks <br />5.764575e-4 months <br /> unless absolutely
i
.necessary.
The Communication Center personnel should be
i
available to provide information needed.
~ '
.
.
This event could have been prevented if the pencil used.to
i-
actuate the level switches had not broken off. ~A metal bolt"
!
has been installed and attached by a chain to the switch,!so-
i
that-it can be inserted and not broken off--inside the switch.
l
Additionally,procedurechangeshave'beenaccomplishedt$
provide cautionary notes to QOS 030-3 and other similar
i
procedures to prevent repetition of this event. Because this
event was identified by the licensee during normal supervisory
reviews and because of the subsequent prompt and extensive ^
j.
corrective actions taken, no violation was issued.
-
.
(6) (Closed) LER 85-021, Revision 00: Unit 2 Scram-Low Level'
.
Indication During Testing.
!.
At 10:45 p.m., on October 15, 1985, Unit 2-was operating in:-the
RUN mode-at approximately-100 percent'of rated core thermal
- "
. power.
Instrument Maintenance personnel were performing
!
" Low-Low Reactor Water' Level Calibration",.when the Instrument
!
Mechanic noticed leakage from an instrument _ tap.: The. leakage
. indicated that one of the isolation valves on a level indicating-
U
j.
switch was-leaking.- When he~ attempted to tighten the low side
!
valve on the switch, the Instrument Mechanic mistakenly cracked
!
- the valve open. He immediately reclosed theivalve. .This action
j
caused a pressure-transient on the instruments connected to this-
l
!
!
'
13' -
,
,
.
.
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-
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.
.
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.
_
_
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.
.
-
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- -
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.
,
~
instrument line. A Reactor scram and Group I,.II, and III
Isolation resulted from.the transient. This event has been
reviewed with the Instrument Maintenance Department as part of
f
their training.
Also,.the station is pursuing continuing efforts to replace the
.
presently installed diaphram-type instruments with analog
,i
devices, wherever possible.
These analog devices are much-less
susceptible to transient pressure spikes.
No further actions
are required at this time.
!'
(7) (Closed) LER 85-022, Revision 00:
Relay Block Dropout causing
{
three quarter Scram Signal While Shutdown
i
"
On October 24, 1985, at 12:36 p.m. Unit 2 was in the SHUTDOWN-
mode. Main Steam Isolation Valves (MSIV) Closure Monthly' Scram
,
!
Sensor Functional Test, were blocked closed per procedure to
i
make it appear as if the condenser was under a. vacuum, because
!
low condenser vacuum can also cause MSIV closure.
Further along
in the test, a one-half scram on the +A'
Channel was being reset
'
'
when the block on a relay fell out. This caused a one-half
scram on the 43' Channel.
This one-half scram on the +B'
i
Channel combined with the half-reset one-half scram on the +A'
}
Channel resulted in a three quarter scram. -The other half'of
l
the one-half scram on the +A' Channel was immediately reset
leaving only.a one-half scram on the +B' Channel.
I
This is the first occurrence of this type, therefore, no-further
j
actions are planned or required at this time.
i
No other violations or deviations were identified.
4
1.
Bulletin Followup
(1) (Closed) IEB 80-07:. BWR Jet Pump Assembly.
'
Nureg/CR-3052 concerning closeout action of.IEB 80-07 was-
prepared by Parameter Inc. under' contract to the NRC. -The NRC
4
i
staff has reviewed the report and concluded that the generic
aspects of jet pump integrity have.been adequately addressed by
!.
licensee corrective measures. The resident inspectors verified
l'
that approved procedures were in place to ensure continued
i
surveillance as follows:
'(a) Individual jet pump flow readings are taken prior to unit
j
startup from a cold condition, and after starting a -
recirculation pump with the reactor.at rated temperature
I
and pressure.
(b) Pursuant.to. the.. Technical Specifications,' recirculation
pump speed and pump' flow are compared' daily tofthe
i
l
characteristic established speed / pump flow curves.' lIf the.
!'
'
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'
'
n,
.
.
).
-
'
'
'14
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- __
-
._
- * - -
.
.
comparison is greater than 10%, a test is performed which
_
compares the indicated total core flow to the total core
l
flow value derived from the established power / core flow .
t
curve.
If this comparison is greater than 10%, a jet pump
l
problem exists.
(c) A daily test is performed similar to item b. above, except
.I
that recirculation pump speed and jet pump loop flow are
!
compared to the characte 'stic established speed / loop flow
!
curves.
If this comparison is greater than 5%, a jet pump
problem may exist.
(d) A daily-jet pump surveillance-test is performed when the-
!
reactor mode switch is in RUN. Individual jet pump' flow
l
readings are recorded.
Normalized flow values are
!
calculated by dividing each jet pump flow reading by the
j
average jet' pump flow for the corresponding recirculation
'!
loop.
These normalized values are compared against the
range of characteristic values.for each jet pump.
If a
normalized value falls outside this; characteristic range,
there may be a jet pump problem.
+
,
The inspector also. verified that visual and ultrasonic
examinations were performed at every refueling outage of the
jet pump beams. Approved procedures are in place to ensure
!
continued compliance.
The licensee does not intend to replace
l
any beams'with the new type.
'
No further actions are required.
-,
2.
(Closed) IE Bulletin 80-25 Operating Problems with Target Rock-
.
Safety-Relief Valves at Boiling Water Reactors
i
s
While Utility personnel responded acceptably on March -17,-1981,
~l
indicating that (a) no corrective action was required for-
l
Actions 1 and 2, (b) modifications were initiated for the
-
'
installation of a relief valve on the drywell pneumatic ~ supply
l
header and (c) an annunciator would be changed, verification of
,
b and c was incomplete or not fully' documented.' The resident-
inspectors have verified that the modifications.have been
completed and that the annunciator change was complete.
Dates
,
"
of the completions were for Unit 1 March 4, 1983'and for Unit 2
1
January 14,~1982.
No further actions are. required.
No violations or deviations were' identified.
j.
Fire Protection
(1) From September 20 to October 21, a routine . unannounced safety:
_
~
inspection in the fire protection area'was conducted by DRSS at
Dresden Units 2 and 3. -Areas included in the' inspection were-
the adequacy of the facilities' Fire Protection program
_
,
15
.
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..
.
=
-
. -- -
.-
- -
.
. ..-
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j-
.
implementation, addressing LERs, and previous Open Items.
t
.
During the course of the inspection it was noted that several-
'
deficiencies were present.
Specifically the deficiency
c
consisted in a failure to comply with a Condition of the License
'
in the area of fire detection.
DRSS, concerned that a similar
problem could exist at Quad Cities,= notified the resident-
.
inspectors of the situation.
The resident inspectors confirmed -
L
,
that a_similar deficiency existed in that the refuel. floor did
'
-
not contain fire _ detection equipment listed in the Safety
Evaluation Report (SER) as required by Technical Specifications.
4
This is a violation as noted in the Appendix (254/85027-09;
265/85030-09(DRS)).
,
,
j
An enforcement Conference was held in theLRegion III' offices on
November 19 at which time the licensee identified additional
- '
discrepancies. -At Quad Cities,'these discrepancies _-included
cable separation concerns and protection'of~ electrical
distribution panels from falling debris.
The licensee will-
1
submit an updated report. listing each discrepancy and the.
I
corrective actions taken or planned.
These actions will be
followed by the resident inspectors.
,
r
2
(2) The Ruskin Manufacturing Company, in a letter to Quad Cities
t
i
dated November 6, 1984, under a potential 10 CFR Part 21,
i
indicated that test methods originally used by Ruskin may not
i
have accurately depicted actual field conditions for dampers
installed inshie ducting.
In addition,.Ruskin stated such
3
'
dampers may also fail to close under actual flow conditions'and
,
l
recommended that Ceco test the dampers for operability.
l
4
Ceco's Station Nuclear Engineering Department (SNED) performed
an evaluation and determined.this condition was not applicable-
i
to Quad Cities as documented on SNED inter-company meno dated
,
j
January 17, 1985.~
A review by a Headquarters NRC inspector'during a special.
i
inspection of the control room HVAC system indicated the
.
,
'
existence of at least one damper (No. CECO 1/2-9472-01) which
j
was required to close under flow due to"its interface with area-
,
smoke detectors and the control room air supply system.
I
The failure to properly and accurately evaluate 'the. original
t
issue raised by Ruskin is considered a violation as noted in the
Appendix (254/85027-10; 265/85030-10(DRP).
-
.
No other violations or deviations were identified.
k.
Regional Requests
Region III_ observed over the course of three inspections of~
!
preoperational testing of the Standby Liquid Control System (SLCS)-
that the involved licensees.were not adequately. implementing the
'
l
'
i
16
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~
-.
.
.
. . -
. - -
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.
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. . . . .
.
testing requirements.of Regulatory Guide 1.68, " Initial Test Programs
for Water-Cooled Nuclear Power Plants." Review of the SLCS
,
preoperational-test at LaSalle, Perry, and Clinton indicated that
testing of the air sparger sub-system was being done improperly.
The testing methodology being employed failed to demonstrate that the
sodium pentaborate solution was being adequately mixed after sitting
for a period of time or that the sampling methodology to be used to
satisfy Technical Specification surveillance requirements would yield
valid results.
Review of'preoperational tests performed at Quad
' '
Cities confirmed that similar tests have been performed. The
licensee is reviewing this situation to determine appropriate actions
.
to take.
Resolution of this issue will be tracked as an Unresolved
Item (254/85027-11; 265/85030-11(DRP)).
1.
Independent Inspection
(1) Recent LERs at other stations have identified several instances
'
where loose electrical connections have been the cause of
'
reactor scrams or other safety system challenges.
The
inspectors reviewed the issue with licensee maintenance-
personnel.
The licensee has committed to review electrical and
inst.ument surveillance procedures and implement changes to.
require periodic checks for loose electrical connectors.
This-
,
will be traced as an Open Item (254/85027-12; 265/85030-12(DRP)).
(2) A design deficiency was identified at the Trojan Station in the
Residual Heat Removal (RHR) System.
Should an RHR pump fail on
demand such that the motor breaker closes.but the pump fails to.
provide flow (e.g. , sheared shaft), its associated mini-flow
recirculation valve would open and provide an alternate. flow _
,
path from the redundant RHR train and starve some of the flow to,
Thus, less water woulu be pumped
into the reactor coolant system than intended during the
.
injection ' phase of a large break loss of coolant accident.
b
The inspectors reviewed the RHR system at the Quad Cities
station and ascertained that a similar. design-deficiency did
not exist.,
,
s
l
(3) During an audit at the Maine Yankee station,.the licensee
,
discovered that pressurizer pressure transmitters, pressurizer
i
level transmitters, and steam' generator level-transmitters >
2
'
!'
were not installed in accordance with manufacturers
!-
recommendations in that the conduit seal assemblies did not-
l
.
!
.have thread sealant applied and may not have been properly.
torqued. Also E.Q. requirements were not factored into.
periodic surveillance procedures. These deficiencies could1
,
invalidate the environmental qualification of the transmitters.
I
,
~ The inspectors reviewed the licensee's actions at Quad Cities-
and verified that thread sealant was.used during installation
l-
I
- 17
-
'
,
-
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and that manufacturers recommendations for surveillance-
requirements were considered. These requirements have~been
incorporated into existing surveillance procedures.
(4) While investigating the cause of failure-of threaded oipe joints
in the fire protection system at Comanche Peak station, the
licensee discovered the presence of Microbiological Induced
Corrosion (MIC), a chemical form of corrosion caused by the
presence of microbes in stagnant water.
To prevent a similar situation at Quad. Cities, licensee procedures
require a system flush twice_per year and a flow test.each year to
verify no degradation. A flo'w test was recently performed and no
indication of piping degradation was found.
No violations or deviations were-identified.
3.
Open Items
Open items are matters which have been discussed with the licensee, which
will be reviewed further by the inspectors, and which involve some action
on the part of the NRC or licensee or both. 'The open items disclosed
during the inspection are discussed in Paragraphs 2.c, 2.d and 2.e.
4.
Unresolved Items
Unresolved items are matters about which more information is required in
order to ascertain whether they are acceptable items, items of
noncompliance, or deviations.
Unresolved items disclosed'during the
inspection are discussed in Paragraphs 2.b and 2.k.
5.
Exit Interview
The inspectors met with licensee representatives (denoted.in Paragraph 1)
throughout the inspection period and at the conclusion of the. inspection
on December 6, 1985, and summarized the scope and findings of the
inspection activities.
The inspectors also discussed the'likely informational content of.the
inspection report with regard to documents or processes reviewed by the-
inspectors during the inspection. _ The licensee _ did not identify any-such
documents / processes as proprietary.
10
.