ML20197B264

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Insp Repts 50-254/97-14 & 50-265/97-14 on 970729-0922.NOV & Deviations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support Re Troubleshooting Resulting in Discovery of Long Standing Problem W/Fire Pump
ML20197B264
Person / Time
Site: Quad Cities  Constellation icon.png
Issue date: 12/16/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20197B025 List:
References
50-254-97-14, 50-265-97-14, NUDOCS 9712230331
Download: ML20197B264 (42)


See also: IR 05000254/1997014

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U. S. NUCLEAR REGULATORY COMMISSION

REGION lli

Docket Nos:

50-254, 50-265

License Nos:

DPR-29, DPR 30

Report No:

50-254/97014(DRP); 50-265/97014(DRP)

Licensee:

Commonwealth Edison Company (Comed)

Facility:

Quad Cities Nuclear Power Ctation, Units 1 and 2

Location:

22710 206th Avenue North

Cordova, IL 61242

Dates:

July 29 - September 22,1997

Inspectors:

W. Kropp, Branch Chief, Reactor Pirjects Branch 1

C. Miller, Senior Resident inspector

K. Walton, Resident inspector

L. Oollins, Resident inspector

C. Lipa, Senior Resident inspector-

Duane Amold Energy Center

R. Gansar, Illinois Depcriment of Nuclear Safety

Approved by:

Mark Ring, Chief

Reactor Projects Branch 1

9712230331 971216

POR

ADOCK 05000254

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EXECUTIVE SUMMARY

Quad Cities Nuclear Power Station, Units 1 and 2

NRC inspection Report No. 50254/g7014(DRP); 50 265/g7014(DRP)

This inspection included aspects of licensee operations, engineering, maintenance, and plant

support. The report covers an 8-week period of resident inspection.

Operations

The licensee identified that on several occasions, operators did not notify chemistry

personnel of the need to perform more frequent sampling of the condenser offgas

system. Similarly, operators failed to test five control rods on Unit 2 prior to raising power

above 40 percent (Sections 01.1,08.7 and M3.2).

The inspectors identified some weaknotses in the licensee's method of counting

50.54(f) indicators (Sections 07.1 and E7.1).

Maintenance

The inspedors found that poor maintenance work practices, including a violation of plant

procedures, prevented conrection of materhl condition problems with an LPCI check

valve. Eventually a leak developed, and repairs resulted in approximately 1 person-rom

additional dose, as well as operational challenges to the plant during a time of operation

with a failed fuel bundle. Poor configuration control and weak understanding of the

design requirements prevented proper alignment of drain valves and prevented

operations personnel from resolving the problem in a timely manner before equipment

had degraded (Section M1.1).

The inspectors' review of the cortpleted surveillance packages verified that the

surveillance results were in compliance with the applicable TS requirements and UFSAR,

but identified that inadequate operations personna' and supervisory review of engineering

surveillance packages had the potential to affect component operability decisions

(Section M1.2).

Maintenance activities resulted in operational disturbances and potentially hazaidous

personnel conditions. Maintenance supervision were hesitant to enter a near miss

situation into the corrective action process. Eventually corrective action processes

worked to the point of identifying hazardous conditions, but failed to come to effective

problem resolution (Section M1.3).

Maintenance activities on the Unit 1 gland steam condenser (GSC) level control valves

(LCVs) were conducted poorly. Problems viith parts support, work package preparation,

planning, troubleshooting guides, work history, and work documentation led to cycling

Unit 1 power levels, increased operator burden, and over 3 person-rem additional

radiation exposure (Section M1.4).

Tne inspectors identified so"eral concems regarding test control during the performance

of the Unit 2 250 Vdc battery modified performance test. The recorded test acceptance

criteria was incorrect and the licensee could not determine where the information was

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obtained. Also, several potential preconditioning issues were identified which could have

affeded test results. The inspectors concluded that the battery test results were

acceptable despite the identified test control weaknesses (Section M3.1).

Even though most surveillances were completed within the critical date, the inspectors

noted a continued adverse trend of missed surveillances. The inspectors concluded that

_ there were multiple reasons for the missed surveillances, Some of these reasons

included defective procedures and/or poor scheduling of surveillances or human error

(Section M3.2).

The inspectors concluded that some TS surveillance requirements and acceptara

criteria were not adequately incorporated into stetion surveillance procedures. The

problems identified were whh a small fraction of the total surveillance population, but the

reviews were conducted on a sampling basis. This could indicate that further -

surveillance adequacy issues remain (Section M3.3).

Enoineenna

The inspectors identified a lack of attention to detail in the design varification process of

calculations for the 250 voit battery (Section E1.1).

Poor communications between engineering. operations, and maintenance personnel were

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evident in backlog reduction efforts (Section E1.2).

The licensee and inspectors identified weaknesses in some safety evaluations

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(Section E1.3).

The inspectots identified that the licensee had not considered the instrument accuracy

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and sensing location in safe shutdown makeup pump system design basis calculations

prior to incorporating the safe shutdown maneup system into the plant TSs. The licensee

did not provide calculations and validate through testing that the surveillance test

acceptance criteria bounded design basis flow and pressure requirements. This resulted

in a violation (Section E1.4).

The inspectors identified various equipment important to safety in an operab,e but

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degraded condition. There were no plans for how and when the equipment would be

removed from the operable but degraded status (Section E2.1).

The inspectors found some discrepancies in the reporting of engineering indicators used

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to support a 10 CFR 50.54(f) request for information (Section E7.1).

The inspectors identified that a licensee commitment made in licensee ovent report (LER)

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50-254/94002 to install a "B" control room emergency ventilation (CREV) hot gas bypass

system had not been met, in August igg 7, the inspectors reviewed tne LER, spoke with

engineering staff, and determined that the system had not been installed and that design

work on the modification had essentially been stopped (Section E8.3).

P! ant Suppgd

An error made by a chemistry technician resulted in a missed TS required surveillance

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(Section R8.1),

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Poor initial troubleshooting efforts and other maintenance problems, such as improper

.govemor installation, prevented the completion of fire pump work within the administrative

LCO time limits. Later troubleshooting resulted in discovery of a long standing problem

.:.with the fire pump. _ Justification forjumpering out fire pump alarms was poor, and '

operator compensatory actions were not adequately spelled out (Section F1,1).

3e inspectors noted an overall lack of sensitivity to fire protection issues. - A number of

equipment problems resulted in administrative Lco time limits being exceeded. Some

equipment was inoperable in excess of 3 years, with planned modifcations to repair the

problems recently canceled or changed. The inspectors noted a lack of rigor in assuring

the required fire watches were established, and a violation was cited. Problem

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identification forms were not effective in focusing management attention on the fire

protection problems. This all occurred in an environment where the licensee was aware

of a relatively high fire risk at the ststion (Section F1.3).

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Report Detalla

Summary of Plard Status

Unit 1 was at full power at the beginning of the inspection period. Fouling of the main

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condenser required the licensee to reduce power daily during off-peak hours to reverse

flow through the main condenser. On September 11 operators reduced power to -

450 MWe to troubleshoot and repair the "B" turbine gland seal condenser level control

valve. On September 16,1997, operators reduced Unit 1 power to about 14 percent to

facilitate a drywell entry to restore the oil level on the 1 A reactor recirculation pump.

Power was held at 400 MWe while repairs were petformed on the 1B gland steam

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condenser level con'tol valve. Again, on September 21, operators reduced power to

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450 MWe to troubleshoot and repair the *B' turbine gland seal condenser level control

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valve. The licensee retumed the unit to full power operations at the end of the inspection

period.'

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Unit 2 was operating at full power at the beginning of the period. A load reduction was'

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conducted on August 6,1997, for drywell entry to identify and isolate a packing leak to the

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drywell equipment drain sump from a core spray testable check valve. Another load drop

was conducted on August 13,1997, while the licensee performed a temporary repair on

the 2A moisture separator drain tank vent fiange. Power increases were rate-limited to

prevent further degradation of a leaking fuel assembly. Hydrogen water chemistry was -

being tripped daily due to offgas oxygen control and offgas hydrogen sampling problems.

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L Operations

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Conduct of Operations

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01.1

Offgas Monitorina Samolina Less Freauent than Reauired by TSs

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Inspection Scope (71707)

The inspectors reviewed operator logs, problem identification forms, and spoke to

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operators

b.

Observations and Findinas

With the Unit 2 oflgas explosive meter inoperable, operators requested that the chemistry -

department obtain grab samples of the ofigas system once every 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> as required by -

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TS Table 3.2.H-i TS allowed relaxing the frequency to once per 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> if reactor power

and offgas recombiner temperature were constant. However, at 10:15 p.m. on

September 4, during flow reversal of the main circulating water system, the hydrogen

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addition system tripped which resulted in a small decrease in recombiner te,mperature.

This condition required a retum to once per 4-hour sampling requirements of the offgas

sptem. Again on September 5 at 8:00 p.m. and at 11:40 p.m., the hydrogen addition

rate changed, requiring more frequent sampling of the offgas system. Operators did not

infoam chemistry of the need to it. crease the offgas system sampling frequency from once

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per 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> to once per 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />. The licensee documented this condition on problem

information form (PIF) Q1ggi-03415.

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This was a Violation (50-254/970141a; 50-265/970141a) of TS Table 3.2.H-1.- The -

- licensee attributed this problem to procedural deficiencies since the system outage report

- does r ot address incrossed frequency of testing on decreased recombiner temperatures.

c.

Conclusions

Operations, along with other departments, failed to meet TS surveillance requirements.

other missed or inadequate surveillances were discussod in Sections M3.2 and M3.3 of

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this report.

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02

. Operational Status of Facilities end Equipment

02.1

Safe Shutdown Makeuo Pumo System Walkdowiis

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Inspection Scoce (IP 37551. 62707. 61726. 71707) .

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The inspectors used Inspection Procedure 71707 to walk down accessible portions of the

safe shutdown makeup syste.n (SSMP). The inspectort reviewed past and recently

completed surveillance tests, QCOS 2900-01, " Quarterly Gafe Shutdown Makeup Pump

Flow Rate Test " maintenance work packages, and correspondence with the

architect / engineering firm for the system,

b.

Observations and Findinas

Review of Surveillance Test Data

.TS ex4ptance criteria were met according to the surveillance test. The acceptance

criteria for this pump were in question due a design basis issue being evaluated by

engineering (Section E1,4) Pump inservice test (IST) vibration readings had been

running near the " alert" level for the past 3 years. The system e'igineer believed the

cause of the vibration was pump misalignment. During recent maintenance activity, a

condition concoming shaft tolerances was identified that could also have been a

contributor to the higher vibrations. The liceasee deferred corrective maintenance to

address alignment and shaft dimensions to a future date.

Review of System Maintenance History

The general condition of the SSMP system was good, with the exception of pump

performance. Earlier Sargeant and Lundy (S&L) engineering data showed that the

SSMP was designed to supply 400 gpm at 1250 psig discharge pressure. Tests

conducted shortly after the system was installed in the mid-1980s showed that the pump

could perform at this level. Records showed that in 1987 the pump seized. Following

seizure, some of the intomal bushings were undercut.- Subsequently, it appeared that the

SSMP pump discharge pressures were typically lower than 1250 psig. Pressure readines

ranged from 1220 - 1240 psig, with several results well below 1200 psig.

Correspondence from S & L to the licensee stated the licensee should check the

accuracy of the installed instrumentation and inspect the pump intemals for the cause of -

the loss in performance. The licensee's records indicated that the instrumentation was -

checked and found to be accurate. However, there were no records to indicate that

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pump intamals were over inspected. The licensee's corrective maintmnoe program :

was weak in that the limitations of the SSMP were not assessed. Subsequently, the

licensee did not aggressively pursue the reduced pressure output of the pump which was

very close to the limit of soceptance. This condstion was documented on Section E1.4 of

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Review of Work Packanes For Recent Maintenance Outane

The pro- and post-job briefing sheets in the reviewed work packages were of several

different revisions. The earlier revisions did not contain control measures to assess

rework afforded in the current work package revisions. Accurate identification of

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maintenance rework had been an ongoing problem at the station for some time.

- Consequently, the licensee had not offectively implemented the necessary controls, to

identify and assest rework conditions into the pre-job briefing. The inspectors assessed

this as an administrative weakness which was acknowledged by the licensee. There

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were no negative consequences to the plant in the cases noted.

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Conclusions

The general material condition of the SSMP system was good with the except!on of pump

performance. Past conduct of maintenance monitoring was insufficient, as evidenced by

the poor monitoring of maintenance history and limited action to correct degraded

SSMP output pressure. There was no evidence that the vendor recommendations to

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inspect the pump intemals were accomplished. In general, the licensee had given the

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SSMP system relatively low prionty in addressing design and equipment issues.

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Quality Assurance in Operationa

07.1

Review of 50.54f Performance Indicators

a.

Inspection Scope

The inspectors reviewed several of the licensee's performance indicators which were

implemented in response to a 10 CFR 50.54f letter from the NRC to Comed. The

indicators included operator workarourids, human performance LERs, and failed TS pump

and valve surveillances.

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Observatioits and Findinas

Ooerator Workarounds

The inspectors reviewed the performance indicator charts for the months of May and

June and noted that the workdown curve had changed. On August 1,1997, the

inspectors obtained a list of scheduled work dates for all the open operator workarounds

(OWA) and compared the OWA list with the workdown curve. The inspectors found that

the workdown curve projected by the work control schedule did not match the work.!own

curve published on the indicator chart and also did not match the workdown curve

projected by the Operations department.

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The inspectors were concemed that the indicator goal of less than 10 percent deviation

from the workdown curve did not appropriately measure progress in reducing the

numbers of operator workarcunds since the workdown curve was changed every month,

1 For example, in May the projected number of OWAs for the end of June appeared to be

' 31. ' :==, the actus: number of OWAs at the end of June was 37, and the goal for

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June was changed to 34. Thomfore, the licensee concluded that the goal was met since

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37 was within 10 percent of 34. (Note that the temporary alteration workdown curve also

changed from month to month). In the future, the licensee no longer planned to change

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the workdown curve monthly.

Human _Pefformancatilcanie1 Event Renoria

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The inspectors questioned the licensee about the goal for the number of human

performance LERs. The goal established was less than or equal to two LERs per month.

The inspectors noted that the numbers of human performance LERs from the licensee's

graph for 1994,1995, and 1996 were, respectively,12, 8, and 17. Therefore,2 humin

performance LERs per month could lead to a total of 24, which would indicate a serious -

decline from past performance. The licensee stated during the August 5,1997,

perfonnance indicator meeting with NRC management that the rate of two LERs per

month was used as a threshold for involving licensee corporate management and not

intended to represent an acceptable level of errors.

Failed TG Pumo and Valve Surveillances

While reviewing the data for this serveillance, the inspectors questioned the high number

of monthly surveillances shown on the indicator chart. It appeared that over

3500 surveillances, were posformed in the month of June. The IST coordinator explained

that control rod drive surveillances and scram time testing of control rods exercised up to

14 valves per control rod (177 total) which were individually counted ir. the total number of

tests. Additionalty, one physical performance of a procedure could account for numerous

component tests (for examp;e; leakage test, valve time test.)

The inspectors reviewed PIFs against the data collected fc.- this indicator and found no

discrepancies. All documented failed surveillances were counted appropriately. It should

be noted that the total number of tests are tracked differently than the total number of

failures. The failures were counted on a per component basis rather than the total -

number of test failures. Since the indicator was being tracked for 6 months prior to

establishing a goal and no rate of failure was calculated, the inspectors concluded that

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there was no impact in counting the failures differently than the total number of tests.

However, if in the future a failure rate was used as a goal, the counting methods would

need to be reevaluated,

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Conclusions

Even though the workdown curves did not accurately reflect the projected rate of reducing

OWAs, the inspectors had noted that the overall number of OWAs had decreased over

the past several months.- The inspectors concluded human performance LERs and failed

TS pumps and valve surveillance indicators were adequately counted.

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Miseellaneous Operations leaues (92700)'

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. 08.1 - (Closed) LER 50-254/94010 00: 50 254/94010-01: Unplanned Scram of Control Rod

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During Surveillance. The surveitance generated a half-scram condition to the reactor -

protection system on Unit 2. Since a half-scram did not satisfy the logic required to

produce control rod motion, control rods on the unit were not expected to move.

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However, Rod D 11 fully inserted. The licensee attributed this event to aged diaphragms

in the 117 scram solenoid pilot valve (SSPV). The inspectors cited the licensee

(Violation 50 254/94017-03; 50-265/94017-03) for ineffective corrective actions for repeat

SSPV problems. The licensee subsequently replaced all SSPV diaphragms on both

units. The inspectors have noted better control rod system posformance. This item is

closed.

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08.2 (Closed) LER 50-254/96001-00: "B" Control Room Emergency Ventilation System

(CREVS) inoperable Due to inoperable Relay. An operator identified the "B" CREV8 fan

was spinning backwards irdcating the fan dampers were open. How long this condition

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existed was unknown. Operators started the system to verify the system was capable of

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meeting its design function. The licensee attributed this condition to a failed relay. No

root cause of the failed relay was identified. The licensee had no plans to periodically

replace the contacts. The inspectors reviewed the licensee's corrective actions. This

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LER is closed.

08.3 (Closed) Inspector Followuo item (IFI) 50-254/96002-03: 50-265/96002-03: Buildup of

Debris on Trash Rock Resulted in Low Water Level inside intake Structure. The low

intake water level condition resulted in the fire pumps becoming inoperable on

January 23,1996. Operators reduced power until the trash rack was cleaned and intake

water level retumed to normal levels inside the crib house. The inspectors were

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concemed that maintenance requests for the system were given a low priority, operators

were not prepared to respond to the event in a timely manner, there was no method to

determine water level inside the crib house and operators did not know what water level

would render pumps incapable of providing flow due to cavitation.

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The licensee responded by revir.ing Quad Cities Operating Procedure (QCOP) 4400-04,

" Traversing Trash Rake," to include a frequency of trash raking and included the minimum

water levels in the bays to ensure various pumps would remain operable. Engineering

confirmed that safety-related pumps would pass the required design flow should the river

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level drop to the Updated Final Safety Analysis Report (UFSAR) specified minimum level

of 561 feet above sea level. However, for inservice testing purposes, the pumps would

be declared inoperable should crib house uter level drop below the level specified la

QCOP 4400-04. In addition, the procedure required operators measure the water level

inside the crib house if the trash rack was dirty and the trash rake was not operable. The

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method for measuring water level was to drop a weighted line until the water surface was

contacted then measure the length of the line. The licenses changed Quad Cities

General Procedure (QCGP) 3-2, " Control of Planned Reactivity Changes," to start TS

required shutdowns in a more timely manner.

Operators continued to monitor trash rack conditions shiftly on rounds. The inspectors

observed trash raking activities during the inspection period and noted the equipment

worked satisfactorily. However, the inspectors noted the depth of water at the north end

of the intake structure was less than 5 feet. The licensee plotted the depth of the water in

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frord of the intake structure yearty end noted the sitt buildup had increased. The licensee t

planned to have the area dredged in the future.- The inspectors noted the sin buildup

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would not inhibit the proper operation of the safety-related pumps should river water level:

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- drop to the minimum UFSAR design water level of 561 feet above sea level.

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The inspectors reviewed the licensee's root cause evaluation, corrective actions, and

procedure changes. This Rom is closed.

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08.4 (Closed) LER 50-254/96006-00: TS 3.0.A Incorrectly invoked. During shutdown of Unit -

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1, operators incorrectly entered into TS 3.0.A to perform a local leak rate test (LLRT).

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The LLRT vented the >rimary containment into secondary containment with the reactor at

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power. The inspectors cited a Violation (50-254/96002-02; 50-265/96002-02) for this -

issue.

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The !!censee attributed this event to an inadequate safety evaluation of the LLRT

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procedure and misinterpretation of the intent and application of TS 3.0.A. The inspectors

reviewed the completed corrective actions listed in the LER. This item is closed.

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' 08.5 (Closed) LER 50-254/97001-00: Missed Operations Surveillances. On January 17,1997,

the licensee identified that two TS required surveillances were missed by control room

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operators. Control room operators changed from 8-hour shifts to 12-hour shifts, but

control room logs were not modified to reflect the shift change. The licensee attributed

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this event to not adequately assessing the change to 12-hour shifts.

The two missed TS required surveillances excesoed the 12-hour limit plus the 25 percent

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alluwed grace period. This was a Non-cited Violation (50 254/96020-01;

50 265/96020-01). The licensee implemented administrative controls to ensure the daily

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surveillances were not missed. This LER is closed.

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08.6 (Closed) LER 50 254/97006-00: Inadequate operations Surveillance. The inspectors

identified that the licenses failed to incorporate four residual heat removal service water

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(RHRSW) valves, which were not locked or otherwise secured in position, in a

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surveillance procedure. The licensee determined the surveillance deficiency was due to

an inadequate procedure development and review due to human error. The inspectors

determined this was a Violation (50-254/97011-03; 50-265/97011-03) of TS 4.8.A. The

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inspectors re, viewed the licensee's corrective actions. This LER is closed.

08.7- (Closed) LER 50-265/97006-00. Missed Control Rod Surveillance. On June 29,1997,

the licensee identified four control rod drives (CRDs) had not been adequately tested prior

to their retum to service. Similarly, on July 16,1997, a fifth CRD was identified by the

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licensee as not having been adequately tested. The licensee declared the CRDs

inoperable, inserted the rods, and satisfactorily tested the CRDs, The licensee attributed -

the missed post-maintenance tests to an ineffective tracking process and human error.

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TS 4.3.D.1 required all CRD testing be completed prior to operating the reactor above 40

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- percent power. At the time of discovery, Unit 2 was operating above 40 percent power.

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The failure to test the five CRDs prior to increasing power on Unit 2 above 40 percent

power was a Violation (50-254/97014-01b,50-265/97014-01b) of TS 4.3.D.1. This LER

is closed.

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08.8 (Closed) LER 50 265/97009-00. Control Room Operators Misread Abnormal Offgas

Rad 6ation Readings. This item was discussed in inspection Report No.50-254/97011;

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50-265/97011. The Irispectors vertfled the control room operator logs had been changed

as stated in the LER. This LER is closed.

IL McIntonance

M1

Conduct of Maintenance-

M1.1 Maintenance Activities

a.

Inspection Scope (61726. 62707)

The inspectors reviewed and/or observed the following work requests (WR) activities and

~-;

.

assessed the workers performance and compliance with plant requirements:

WR 970081320

Unit 1 Emergency Diesel Generator Monthly Load Test

+

WR 96003387401

Repair of 2A low pressure coolant injection (LPCI) air

.

operatsd check valve.

WR 970074951

Install / Remove Jumper in Unit 2 Rod Control System

.-

WR 970089249

Replace Unit 2 Main Steam Line Square Root Converters

+

b.

Observations and Findinas

!

On August 6,1997, Unit 2 reactor power was reduced in order to troubleshoot and repair

a valve packing leak in the drywell. The inspectors reviewed maintenance records and

design information involving valve repacking activities to determine the appropriateness

of the activity and the rotationship to later packing failure. The inspectors' review

determined that about 1 person-rom of exposure resulted from the downpower and repair

activities for the 2A LPCI air operated check valve. The inspectors leamed that the valve

had previously been mpacked in March 1997, Work Request 96003387401 was

performed in March 1997 and included inspection and repair activities on

LPCI Check Valve 2-100168a. After reviewing Work Request 96003387401, the

'

Inspectors discovered that the instructions in the maintenance request were not property

f

followed, and that the design of the packing leak off line for the valve was not understood

by plant personnel.

,

'

Work Request 90003387401 was written to allow for packing replacement. The

supervisor involved changed the scope of the request to add packing rings vice replace

packing, without properly changing the procedure. The work request referred workers to

Attachment D of mechanical maintenance procedure Quad Cities Mechanical

Maintenance (QCMM) 1515-07, Revision 7, " General Valve Packing Procedure." The job

supervisor, when interviewed, indicated that although the package required changing out

i

the inner und outer packing, he did not think that was necessary for the scope of the job.

instead of following or properly changing the procedure, the supervisor elected to only

,

,

add rings to the outer packing, reasoning that there was no indication of packing leakage.

l

However, the inspectors noted that the outer packing was being replaced because ti. ore

was no adjustment left for tightening packing due to previous tightening efforts - an

indication of packing leakage. By adding rings to the outer packing, the supervisor was

'

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also potentially adversely affect.ng the two stage packing with leak-off line arrangement.

TS 6.8.A required applicable procedurcs recommended in Appendix A of Regulatory

Guide 1,33, Revision 2, February 1978, be impleinented. This regulatory guide included

i

administrative procedures dealing with procedure adherence and maintenance

procedures dealing with safety-related equipment. Failure to follow procedure OCMM

1515-07 was a Violation (50-265/97014 02) of TS 6.8.A.

Following plant startup, the inner packing began leaking and eventually resulted in a unit

d-rwrpr;r to isolate the packing leak. The packing leak was routed through a leak-off

line which led to the drywell equipment drain sump. The excessive leakage required

frequer:t pumping and recirculation of tne sump. In addition, the high temperatures

'

caused by the leak eventually led to a required change out of the sump pumps. These

operator problems and the radiation dose received from the rework on this job could have

been avoided had the original maintenance activity been conducted property.

+

Once the leak was discovered, operators could not tell if the leak-off line was supposed to

be open or closed. The leak-off line isolation valve 21001-64c for the 68a check valve

was shown by piping and instrument diagrams (P&lD) to be open but required by

Qusd Cities Operating Mechanical (QOM) 2-0020 02, "U2 Drywell Valve Check List,"

procedure to be closed. The isolation valves had been listed as a discrepancy in the

QOM check list, and left open. Failure to control plant configuration property, and

property evaluate procedure changes led to the increased leakage into the drywell

' *

equipment drain sump. The licensee addressed the discrepancy by initiating

Drawing Change Request 970179 to change the indicated position of the valve to

" closed" on the P&lD. This licensee-identified and corrected violation is being treated as

a Non cited Violation (50-254/97014-03; 50-265/9701443) consistent with

- Section Vll.B,1 of the NRC Enforcement Policy. The inspectors found through

discussions with engineering and maintenance personnel that drywell equipment leak-off

drain lines were initially installed to give early indication of packing leakage. Inability to

maintain packing was cited as the reason for plant decisions to isolate the leak-off

isolation valves, and even cap off the lines in some cases. Poor understanding ofine

design configuration led to a situation where degraded I;acking and an open drain line

caused an excessive amount of drywell packing leakage.

c.

Conclusions

4

The inspectors found that poor maintenance work practices including a violation of plant

procedures prevented correction of material condition problems with a LPCI check valve

and resulted in approximately 1 person-rem additional dose, as well as operational

challenges to the plant during a time of operation with a failed fuel bundle. Poor

configuration control and weak understanding of the design requirements prevented

proper alignment of draic, valves and prevented operations from resolving the problem in

a timely manner before equipment had degraded. A non-cited violation was issued

'

following licensee identification and resolution of the configuration control problem.

,

1

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l

M1.2 Surveillance Observations

a.

Insoection Scoce

The inspectors reviewed and/or observed the surveillance activ.cas listed below. The

inspectors verified the surveillances were in conformance with the design basis of the

facility and in compliance with TS.

QCOS 0300-01

Control Rod Drive Exercise

QCOS 1000-06

Quarterly Residual Heat Removal (RHR) Pump / Loop Operability

Test

QCOS 6900-01

" Station Battery Weekly Surveillance" for March 11,18, and 24,

1997, for the Unit i Safety-Related 250 Vdc Battery

QCOS 6900-02

" Station Battery Quarteriy Surveillance" Performed on the Unit i

250 Vdc Battery on March 14,1997

QCOS 6900-02

" Station Battery Quarterty Surveillance" performed on the Unit 2

250 Vdc Battery on March 31,1997

QCTS 0240-04

" Unit One (Two) Service Test 250 Vdc Safety Related Battery"

Performed on the Unit i 250 Vdc Battery in May 1996

QCTS 0240-06

" Unit One (Two) Modified Performance Test 250 Vdc Safety

Related Battery" Performed on the Unit 2 250 Vdc Battery on

April 7,1997

b.

03servationt_and Findinas

During this review the inspectors identified concems with the surveillance procedures

pertainog to testing methodology and the accepte. .e criteria used in procedure

Quad Cities TS (QCTS) 0240-06 " Unit One (Two) Modified Performance Test 250 Vdc

Safety Related Battery," Revision 2. These concems are discussed in detailin

Section M3.1 of this report.

The inspectors also identified a concem with the review process of completed

surveillances. Surveillance procedure QCTS 0240-06 did not require a review of the test

results by on-shift operations personnel prior to declaring the 250 Vdc battery operable.

The inspectors were concemed that only one level of review of completed surveillance

packages coeld lead to unacceptable surveillance results not being identified in a timely

manner prior to declaring a component operable. For example, TS surveillance

QCTS 0240-06 perfrvmod on April 7,1997, and discussed in Section M3.1 of this report,

had an incorrect acceptance criteria for the battery capacity. The acceptance criteria was

required to be noted in Step D.8 of the proc 3 dure each time the modified performance

test was performed by engineering. The inspectors identified there was no operations

review of the cumpleted package; therefore, there was a missed opportunity to identify

the incorrect acceptance criteria on April 7. The incorrect acceptance in this casa did not

resultin an inoperable battery,

13

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- c.

Conclusions

The inspectors' review of the completed surveillance packages verified that the

surveillance results were in compliance with the applicable TS requirements and UFSAR,

but that inadequate operations and supervisory review of engineering surveillance

packages had the potential to affect component operability decisions.

<

k 1.3 Eg[R100tllEftbLEt9 Meet

a.

Insoecuon scope

The inspectors rev wwod plant response to two events involving maintenance activities

which had a high potential for, but fortunately did not resuh in personnel injury,

b.

Observations and Findings

in one case, on August 13,1997, inspectors observed maintenance personnel

conducting fire system surveillance Quad Cities Mechanical Maintenance Surveillance

(QCMMS) 4100-32, *1/2A-4101 Diesel Driven Fire Pump Annual Capacity Test." Just

prior to opening a fire test header isolation valve, two maintenance supervisors walked

onto a catwalk over the circulating water discharge canal to test the structural integrity of

devices installed to protect plant equipment from damage caused by high pressure water

sprayed during the surveillance. When the valve was opened, high pressure water

trapped in the line discharged into the discharge canal area and struck one supervisor,

pushing him up against a safety railing and knocking his hard hat into the discharge

'

canal. The procedure and maintenance supervision failed to adequately protect

personnel from injury during the surveillance activity. Additionally, this near-miss incident

was net documcnted on a PIF until prompted by the quality and safety assessment

mar ~ dr the following day.

Corre,

e action for the event was also inadequate in that PlF Q1997-3188, written to

address the problem, did not adequately address the safety issue involved. The PlF was

closed to a data point with the understanding that a change to the surveillance procedure,

including an additional caution statement, would be made. However, on September 2

i

when the inspectors reviewed the QCMMS, a correction to the procedure had not been

i

made. in addition, the PlF had identified that the likely cause of the pressure surge when

,

opening the system was water trapped due to valve leakage into the header. But

corrective action to fix the valve leakage had not been taken or initiated as of August 29

'an the inspectors informed plant management. On September 2 the valve work was

not p',rformed and the procedure change had not been implemented, meaning that no

. -

effective corrective action had yet been taken. Following NRC discussions with

management, operators hung caution tags on the valve in question to assure personnel

safety until the issue was resolved.

On September 2,1997, the inspectors observed control room operations and

maintenance staffs respond to an event in which workers cut a live 13.8 kV electric line

by accident using a backhoe. This event was very similar in nature and consequences to

-

another 13.8 kV line cut caused by maintenance on September 9,1996, and documented

,

in Inspection Report No.254/96012; 50-265/96012. Operators properly addressed the

numerou annunciators and equipment changes cau' sed by the high voltage line cut, but

j

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were distracted from routine control room duties during the event.E The inspectors found

that tne workers had made attempts to locate energized lines in the dig area. The

licensee was investigating the cause of the event, using PIF Q1997-03367 as the tracking

mechanism,

c.

Conclusions

The inspectors concluded that maintenance activitievosulted in operational

distutt>ances and F-ME'"i hazardous personnel conditions. Maintenance supervision -

were hesitard to enter a near miss situation into the corrective action process. Eventually

corrective action processes worked to the poird of identifying dangerous conditions, but

failed to come to effective problem resoluti,m.

M1.4 Poor Gland Seal Level Control Valve Maintenance

a.

. inspection Scope

The inspectors reviewed work packages and work in progress to determine the

effectiveness of maintenance in repairing the "1B" gland steam condenser (GSC) level

control valve (LCV.)

b.

Observations and Findinas

4

The gland seal condenser level control valves have been chronic maintenance problems

at Quad Cities in the recent past. The Unit 2 startup from the Q2R14 refueling outage

was troubled by GSC LCV problems. The 1 A GSC LCV had been tagged inoperable

since April 1997.. Maintenance history showed problems with the 1B valve in

November 1996 and then in January 1997, June 19g7, and then August through

September 1997. Radiation dose to workers had been high when failures occurred

because the area of the LCV was a high radiation area during power operations. The

system was designed with redundancy, so when one LCV failed, the o'her may be put

into service. However due to inability to maintain the valves, Quad Cities has been

operating Unit 1 with only one operable LCV. Thus when the 1B valve began to fail in

~ August 1997, operstc. s were forced to go into the heater bay to manually control

.

GSC level. Inability to control level could have resulted in gland steam leaks in the heater

bay on high level, or degraded main condenser vacuum on low level.

Operations normally reduced reactor power in order to lower radiation exposure to

operators and maintenance workers when a GSC LCV problem was experienced.

Although as low as reasonably aciiievable (ALARA) practices were normally followed for

the repairs, the number of repair attempts led to high overall exposures to personnel in -

August and September. Radiation exposures of up to 3.5 person rem were experienced

for all the various heater bay entries involved.

The inspectors noted that the initial work package for repairing the 1B GSC LCV lacked a

troubleshooting plan. Several attempts were made to repair the valve by tuning the -

controller, repairing air leaks, and repairing a valve diaphragm, before a comprehensive

plan was a developed by a team. The inspectors spoke with Me maintenance

i

superintendent who indicated that this effort did not meet hb expectation for a

..

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A

troubleshooting plan. That expedation had been expressed earlier following poor -

maintenance on diesel generator air start motors.

,

The inspectors noted that some of the entries in Work Package 960102229 lacked detail.

Previous attempts to repair the LCV were recorded with insuffderd h! story to determine

the problem with the equiomord. During the repair attempts on the 1B valve,

maintenance and engineering personnel also attempted to repair the 1 A valve. Partly due

to insufficient documerdation of the status of the 1 A valve, there was significant confusion

about the status of the valve, leading personnel to spend effort on the repair when a

retum to service was unlikely.

Parts support ws: =!:o a oroblem. Techniciam found that parts on order to mpair the

1B valve were incorrect. Once the 1B valve intomats were removed, incorrect parts were

also found there. The inspectors were also informed that parts to repair both the

1 A valve and the 1B valve were not available. The inspectors questioned why a critical

balance of plant component with por repair history did not have ample spare parts

available to fix both the 1 A and 1B LCV, especially considering the two active

maintenance requests written against LCVs on Unit 1 and Unit 2.

c.

Conclusions

Maintenance activities on the Unit 1 GSC LCVs were poor. Problems with parts support,

work package preparation, planning, troubleshooting guides, work history, and work -

documentation, icd to cycling Unit 1 power levels, increased operator burden, and

additional radiation dose.

M3

- Maintenance Procedures and Documentation

Qggd Cities Techrical Staff Procedure 0240-06. " Unit One (Two) Modified Performance

l

M3.1

Test 250 Vdc SafeN Related Batterv"

a.

Inspection Scoce (61726)

The inspectors had previously witnessed portions of the Unit 2 modified performance test

for the Unit 2 250 volt direct current (Vdc) safety-related battery conducted in accordance

with QCTS 0240 06 on April 7,1997 (see inspection Report No. 50-254/97006(DRP);

_'

50-265/a7006, Section M2.3). During this inspection, the inspectors further compared the

completed test package to the designed load duty cycle of the battery to verify that the

test requirements conformed to TS 4.9.C, UFSAR 8.3.2.1, and S&L battery calculation,

"PMED 891377-01", Revision 10. The inspectors had specific observations pertaining to

PMED 891377-01 which are discussed in Section E1.1 of this report.

b.

Observations and Findinas

The review of the completed April 7,1997, modc id performance test package

(QCTS 0240-06) identified several issues, some pertaining to methodology and others to

acceptance criteria. The updated TS, issued in the fall of 1996,' allowed the licensee to -

conduct a modified performance test on the 250 Vdc battery in lieu of a separate service

test (based on the battery's design duty cycle) and a performance test (measures battery

capacity). The requiremer,ts for a modified performance test is defined in standard

-

Institute of Electronic of Electrical Engineers (IEEE) 4501995, " lEEE Recommended

practice for Maintenance, Testing, and Replacement of Vented Lead-Acid Batteries for

%

16-

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Stationary Applications." The licensee issued procedure QCTS 0240 06,

" Unit one (Two) Modified Performance Test 250 Vdc Safety Related Battery," to define

the testing methodology for the new TS modified performance test.

- The inspectors identified the following concems with the April 7 modified performance

test and procedure QCTS 0240-06:

Step D.8 of procedure QCTS 0240-06 required the individual performing the test

to determine the minimum acceptable battery capacity from the latest revision of

the direct current (dc) Electrical Load Monitoring System (ELMS) and record the

number in the step. The minimum acceptable battery capacity acceptance criteria

recorded for the April 7 test was 70 percent. This acceptance criteria was not

correct. The minimum acceptable capacity should have been 80 percent or the

margin calculated from the design load profile for the battery, whichever is greater

(Step F.4). In the case of the April 7 modified performance test, based on the

current capacity margin as defined in the design load profile, the minimum

!

capacity acceptance criteria should have been 80 percent. The completed

modified performance test determined that the battery's capacity was 100 percent;

'

therefore, the incorrect acceptance criteria of 70 percent did not adversely impact

the operability of the battery. The licensee could not determine where the

70 percent acceptance criteria was obtained. The failure to have the correct

acceptance criteria for the Unit 2 safety related 250 Vdc battery modified

performance test is considered a Violation (50-254/97014-04; 50 265/97014-04)

of 10 CFR 50, Appendix B, Criteria XI, " Test Control."

l

Section B of proc 4 dure QCTS 0240-06, titled " Discussion," stated the initial

i

e

'

conditions for the modified performance test should be identical to those specified

for a service test. Also, IEEE 450-1995, Ssetion 5.4, had a similar statement.

I

'

Procedure QCTS 0240-06 referenced standard IEEE 450-1987 which was

incorrect since it did not address modified performance testing. For the purpose

of this inspection, the inspectors utilized IEEE 450-1995 as t'l* recognized

standard for the modified performance test.

The purpose of a service test was to determine if a battery could provide the

required current within specified voltage parameters during the design load profile.

Standard IEEE 450-1995, Section 6.6, stated that the battery condition for the

service test be in an "as found" condition. For example, battery connections and

'

resistance readings can be checked prior to the test, but no corrective action

would be taken unless there was a possibility of battery damage. The inspectors

identified the following concems in this area:

(1)

On March 31,1997, the licensee performed TS 4.9.C.2. Quad Cities

Operations Surveillance (QCOS) 6900-02, " Station Battery Quarterly

Surveillance." During the surveillance, corrosion was identified at cell

connections 70,73, and 90. Procedure QCOS 6900-02 required the

corrosion to be cleaned by performing procedure Quad Cities Electrical

Preventive Maintenance (QCEPM) 0100-01, " Station Battery Systems -

Preventive Maintenance." The inspectors determined that the corrosion

was cleaned from the affected cells. - The inspectors reviewed the records

i

associated with the recording of the cell resistance (Attachment F of

17

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-

,

r

procedure QCEMP 0100-01) and noted that only "as found" resistance '

,

readings were recorded and not also the "as left." The inspectors were

concemed that the battery was not tested on April 7 in the "as found"

condition as recommended by lEEE 4501995.

(2)

The modified performance test procedure QCTS 0240-06, Revision 2, did

not require that all battery connections have the correct resistance. The

inspectors determined that the last time the resistance of the battery

connections were checked was in May 9,1996, approximately 11 months -

prior to the April 7,1997, modified performance test. The resistance was

checked as required by TS 4.9.C.3 using procedure QCEMP 0100-01,

" Station Battery Systems Preventive Maintenance." The TS surveillance

was to be performed every.18 months. The inspectors were concemed

that the "as found" condition of the battely was not being ascertained prior

to performing the modified performance test as recommended by

lEEE 4501995,

A prerequisite, defined in Step D.6, stated that if necessary, locate temporary

e

heaters in the battery room to mainta!n adequate electrolyte temperature. The

procedure did not identify the adequate electrolyte temperature

(note: TS 4.9.C.2c. requires the average electrolyte temperature to be above

-

60'F). Even though heaters were not used prior to the April 7 modified

performance test, the inspectors were concemed that using heaters in the future

would be preconditioning the battery for the portion of the modified performance

test pertaining to the 1 minute peak testing discharge rate (920 amps), increasing

the electrolyte temperature improves the battery's performance and could mask a

degraded battery and coiTipromise the requirement of testing the battery in an "as

found" condition. This concem was discussed with the licensee, and procedure

QCTS 0240-06 will be revised to delete placing heaters in the battery room to

elevate the battery's electrolyte temperature prior to the test.

'

Conclusions

The inspectors identified several concems regarding test control during the performance

of the Unit 2 250 Vdc battery modified performance test. The recorded test acceptance

criteria was incorrect and the licensee could not determine where the information was

obtained. Also, coveral potential preconditioning issues were identified which potentially

could have affected test results. The inspectors concluded that the battery test results

were acceptable despite the identified test control weaknesses.

M3.2 Missed Surveillances

3

a.

inspection Scope (92701,61726)

The inspectors reviewed recent PIFs and LERs associated with missed surveillances.

b.

Observations and Findinas

.The hspectors noted multiple instances of missed surveillances identified by both the

i

licensee and the inspectors over the past year. In the winter of 1997, the inspectors

_

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,

identified two violations where control room ventilation surveillances were missed. These

were due to inadequate review of existing surveillance procedures to ensure the new

TS upgrade program (TSUP) requirements were included. More recently, the inspectors

identTHHi two non-cited violations (NCVs) for missed surveillances. One of these missed

surveillances was due to operators changing from 8-hour to 12-hour shifts (see Section

08.5). A second NCV cited a deficient localleak rate test identified by an NRC

information notice (see Section E8.9). Both NCVs were attributed to different causes,

in this report, five miswed inservice testing surveillances resulted in a violation

(see Sections MB.3, M8.4 and E8.13). The licensee attributed two of these to defective

procedures. A third missed surveillance was mostly due to a scheduling process

deficiency A failure to test five control rods before Unit 2 power was increased above

40 percent was attributed to post rnalntenance testing process deficiencies and human

erm (see Section 08.7) A missed chemistry surveillance was att-ibuted to human error

(see Section R8.1).

The licensee recently documented two PlFs where non TS required surveillances were

not completed on the scheduled dates due to scheduling deficiencies. A room cooler

inspection was deferred numerous times due to scheduling conflicts (PIF Q1997-3452).

A computer room halon surveil lance exceeded its critical date due to scheduling

deficiencies (PlF Q1997-3447),

c.

Conclusions

Even though most surveillances were completed within the cri ical date, the inspectors

noted a continued adverse trend of missed surveillances. The inspectors concluded that

there were multiple reasons for the missed surveillances. Some of these reasons

included defective procedures and/or poor scheduling of surveillances or human error.

M3.3 Inadeouste Surveillances

a.

insoection Sqqp3 (92701,61726)

The inspectors reviewed LERs, PIFs and surveillance procedures to ensure TS-required

surveillance tests were properly implemented,

b.

Observations and Findinas

- The inspectors noted four instances of inadequate surveillances. A battery surveillance

lacked the correct acceptance criteria (see Section M3.1) Additionally, a

RHRSW surveillance was inadequate to assure equipment operability (see Section E8.5).

A safe shutdown makeup pump surveillance was lacking design basis documentation

(see Section E1.4). An operations monthly surveillance failed to include four

RHRSW valves (see Section 08.6).

c.

Conclusions

rhe inspectors concluded that somo TS surveillance requirements and acceptance

criteria were not adequately implemented into station surveillance procedures. The

problems identified were with a small fraction of the total surveillance population, but the

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reviews were conducted on a sampling basis. This could indicate that further

survelilance adequacy issues remain.

MS

Miscellaneous Maintenance issues (92902)

M8.1 LQhaed) LER 50-26: Misinterpreted TS Surveillance

Requirement. As discussed in Inspection Report 50-254/96012; 50-265/96012, the

licensee originally believed that a TS required surveillance was missed; however, upon

further revisw, the licerssee determined that no surveillances were missed. An Unusuel

Event was declared and terminated on September 4,1997, and was subsequently

,

retracted on September 1E 1997. The licensee submitted the LER voluntarily to report

the event. The inspectors agreed with the licensee's determination that no TS

surveillances were missed and had no further concems. This item is closed.

M8.2 [Q!osed)IFl 50-254/97006-05@f.5197006-Q1: Unit 2 250 Vdc Battery Modified

Performance Test Load Profile. Th9 inspectors further reviewed the load profile and

determined that the high pressure coolant injection (HPCI) suction path transfer from the

contaminated condensate storage tank (CCST) to the suppression pool was adequately

modeled. Also, all safe shutdown loads were included in the load profile. Additional

inspections were performed on the 250 Vdc battery system and the results are

documented in section M3.1 of this report. This item is closed.

MB.3 (Closed) LER 50-254/97014-00: Target Rock Mfety Relief Valves (TRSRV) Did Not

Receive As-found Set Point Testing Within 12 Mcnths. The licensee identified that

neither Unit 1 nor Unit 2 TRSRVs that were removed during the most recent unit refuel

outages, had been set pressure tested within 12 months of their removal from the

system. The licensee had since set pressure tested both TRSRVs. Both valves were

outside their 1 percent acceptance band and were adjusted. The licensee evaluated the

as-found condition as a condition not violating any reactor safety limits or fuellimits. The

licensee attributed this event to defective procedures which failed to ensure prompt

testing of tue TRSRVs. Similar procedure deficiencies were identified with the main

steam safety valve (MSSV) testing. The inspectors noted the le.ensee planned to modify

TRSRV and MSSV testing procedures.

The relief valves were required by TS 4.0.E and American Society of Mechanical

Engineers (ASME) Code requirements to be set pressure tested withiri 12 months of

removal from the system. Failure to set point test the valves within the nquired time was

a Violation (50-254/97014-01c; 50-265/97014-01c) of TS 4.0.E. This LER is closed.

Ma.4 [ Closed) LER 50-254/97016-00: Diesel Generator Cooling Water Inservice Testing

Requirements not Completed. Licensee operating surveillance procedure,

QCOS 6800-08, * Quarterly % Diesel Generator Cooling Water (DGCW) to Unit 1 and

Unit 2 ECCS (Emergency Core Cooling System) Room Coolers Flow Test," was intended

to be performed for both units. However, the licensee's scheduling process tested Unit 2

components, but did not schedule the test for Unit 1 components. Afterwards, the

licensee completed the surveillance for Unit 1. The licensee issued two predefine work

requests for the surveillance test.

This surveillance test was required by TS 4.0.E , inservice testing and inspection of

ASME Code Class 1,2, and 3 valves. The failure to complete QCOS 6600-08 for Unit 1

20

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__________ _ _____ _ _____ _ _ - _ -_______ _____ - ______- _ - __ _ __ _ _ - -

for the second quarter 1997 was a Violation '50 254/97014 01d; 50-265/97014 01d) of

TS 4.0.E. This LER is closed.

Ill. Enn'neerina

E1

Conduct of Engineering

hpl.gs1Qttga_Ir,formajion Tran1mittals SO40 Oll-0296 AND 0302

i

E1.1

,

s.

kapt@_qnSoppa f71707. 37501)

The laspectors reviewed Nuclear Design Information Transmittals (NDITs)

SO40-QH-0296, dated February 14,1997, and SO40 OH-0302, dated Mare.h 4,1997, to

verify compliance with TS and UFSAR requirements. Nuclear Design Information

Transmittal SO40-QH-C296 evaluated battery loads based on abnormal operation of the

Units 1 and 2 HPCI emergency oil pumps and the Unit i HPCI tuming gear. Nuclear

Desi- t Information Transmittals SO40-QH-0302 evaluated the effects on the Unit 1

safety-related 250 Vdc battery with Unit 1 at power supplying 250 Vdc busses 1,1A,18,

2A and 28 a!ong with the Unit 2 safety-related 250 Vdc battery undergoing a service test.

Each of thess NDITs had Sargeant and Lundy (S&L) calculations attached to support the

conclusions documented in the NDITs.

b.

Observations and Findinas (b1726)

Calculation PMhD 891377-01, Revision 10, dated March 4,1997, identified a change to

the most limiting load profile on the Unit 1 & 2 *250 Vdc Safety Related Batteries' as a

main steam line break outside containment. Previously, an intermediate loss of coolant

accident was considered the most limiting case. The inspectors reviewed supporting

documentation within calculation PMED 891377-01 and identified the following conc.ims:

The battery Flzing calculations, dated Fcruary 13,1997, that were included in

e

NDIT SO40-QH-0296 utilized 65T. as tha lowest expected electrolyte

temperature. The correction factor of 1.08 for this electrolyte temperature was

used in uetermining the number of positive plates required for the battery to meet

the design load profile. However, updated TS 4.9.C, issued in the fall of 1996,

identified the lowest electrolyte temperature as 60', which required a temperature

correction factor of 1.11, Thereforo, by using the 1.08 factor versus 1.11, the

sizing calculations were non conservative. The use of the incorrect temperature

did not reduce the battery capacity margin a significant amount, and the

safety-related 250 Vdc batteries remained operable. The use of the wrong lowest

expected electrolyte iemperature as a design input to o battery sizing calculation

was si Violation (SJ-254/97014-052; 50 205/97014-05a) of 10 CFR 50,

Appendix B, Criterion lil, " Design Control."

The worst case 250 Vdc battery load profile was based on assumptions in

e

calculation PMED 891377-01, Revision 10. One of the assumptions used in the

calculation was the failure of the unit emergency diesel generator (EDG).

However, in 1993 the de turbine emergency oil pump (EOP) was removed as a

load from the safety-related 250 Vdc battery and placed on a nonsafety-related

21

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,

banery. Calculation PMED Sg137741 was revised to remove the de turbine EOP

from the battery load pronie. However, the review and design vert 6 cation of the

ravised Ma%, and other subsequent revisions, failed to idenufy that with the

'

unovel of the dc turbine EOP the failure of the M (swing) EDG would result in

the worst case pronie. The assumed failure of the M EDO would resuM !n the

I

unintermptible power supply (UPS), a 7G amp load, being powered from the

j

C:Fi::f 250 Vdc battery. The failure to idenufy a change in a design basis

assumption in 19g3 due U a mod 46 cation was another example of a

'

Vleistion (50-254/97g1445b; 50-285/97014 05b) to 10 CFR 50, Appendix B,

-i

'

CrNorton lil, * Design Control.'

The inspectors noted that station engineering persegnol did not have a thorough

c

understanding of the design basis of the aatety-related 250 Vdc battery system.

l

'

Questions regarding the loart proRio and the test soceptance critoria were initially posed

'

to the engineering staff in April, shortly after the test was performed. However, complete

answers were not provided to the inspectors until August. Battery sir.ing and load pronle

coloulations were performed by S&L and M appeared to the inspectors that transmitted

i'

data and results required for the testing did not recolve an in-depth site engineering

review prior to use.

t

'

c.

Conclosigns

Errors in 84L calculation PMED 8g1377-01 were indicative of a lack of attention to detail

in the design verification process of calculationc. Other minor problems were identified

with the calculation and the NDITs (that is; wrong calculation referenced, clarity, etc.) that

also substantiate the need for management attention in engmeeting activities. The

<

licensee has recently established a engineering assurance group (EAG) in April igg 7.

,

Part of the EAG's responsibilities would be to perform a sample review, as an overview

function, of calculations. Due to the EAG's recent establishment, the effectiveness of the

'

EAG could not be determined.

,

.

The inspectors considered the change to the limiting load profile of the 250 Vdc battery

system to be important design basis information and expected that station engineering

personnel would have detailed knowledge of the design basis.

But in addition to lack of attention to detailla the design verification process, the

inspectors were concemed that station engineering personnel did not have a thorough

understanding of the design basis for the safety related 250 Vdc battery system. This

was evident by the initial inability to answer questions regarding the limiting load profile

for t'i s 250 Vdc battery system and the length of time to provide answers to those

- questbns.

E1.2 Poor Comrpunication in Backlog ReductienEfforts

i

s.

Inspection.8 cope (71707)

The inspectors reviewed a list of engineering requests which had been canceled by

engineering, to determine impact en other departments.

.

.

2

22

J-

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.-2.

. = - ,. - ,~ :.-- - . - - ~ .~.-... - .. - .,. - .. - . _ .. - .,. - ,.- . ,- . -.. _ _ _ - - , - . -

c,-

..

b.

Observations and Findinas

During the review, the inspectors leamed from a supervisor in another department that an

engineering request he was counting on for cathodic protection system improvements

had been canceled without his knowledge. The inspectors spoke with plant management

representatives who later indicated that the engineering requests had been cav.eled

inappropriately and without proper review by Operations. Some of the engir eering

requests which had not been reviewed by Operations for cancellation included HPCI push

button start modification work,1 A air ejector booster modification, heat tracing for diesel

fire pump lines, and hot short protection valve bgic modification.

The inspectors learned of another backlog reduction effort which involved engineering

requests, action requests, nuclear work requests, PlFs and other items with high backlog

numbers. A team was formed this period to reduce these backlog numbers with such

intended methods as the screening team voting on canceling old nuclear work requests

and engineering requests, and deleting nuclear work requests from the maintenance

backlog when there was an engineering action associated with the request. After further

managiment review, the licences decided not to delete work requests from backlog

numbers simply because a supporting engineering request was needed.

c.

ConclusioD.1

The inspectors found that station management was not fully aware of the nature of the

backlog reduction screening efforts being attempted, and that Operations did not have

sufficient understanding of the process to ensure that required items were being properly

tracked and not inappropriately canceled. Poor communications between engineering,

operations, and maintenance personnel was evident in both backlog reduction efforts.

E1.3 quality of Enalneerina Safety Evaluations

a.

Agapection Scong (37551)

The inspectors reviewed various safety evaluations and screenings associated with

maintenance and surveillance activities. The inspectors also reviewed vnrious PlFs and

temporary alterations.

b.

Observations and Findinal

Control Rod Drive P-4

The inspectors observoo Unit 2 opteators perform weekly control rod surveillance tests.

However, a poor electrical contact in the control rod logic circuit inhibited operators from

moving control rod P-4. In order to complete the surveillance test, operators reques%l

maintenance personnel to install a jumper around the poor electrical contact. Since

late July, maintenance personnel controlled the installation and removal of the jumper

with a work package and Quad Cities Instrument Procedure (QCIP) 100-13, Ma'.ntenance

Alteration Procedure." Maintenancs questioned whether the practice of installing and

removing the jumper weekly bypassed the more cumbersome temporary alteration

process. The licensee documented t.ie issue on a PIF Q1997 3290.

23

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_

__

The inspac. tors noted this practice did not inhibit control rods from scramming but resalted

in periodicalty blowing of a % amp power supply fuse. The inspectors also noted this

condition was not listed on the operator work around list. However, the licensee planned

to correct the deficient condition during the upcoming planned maintenance outage, in

response to the PlF, operations changed QCOP 0300-01 to sequence and control

installing and removing the jumper. Subsequently, operators imerted Rod P-4 and took

the rod out of service to avoid the need of installing and removing the jumper from the rod

control system.

The inspectors consider the addition of a jumper to the rod control system to be a change

to the facility as oescribed in the UFSAR and required 10 CFR 50.59 screening to

determine if the addition of the jumper constituted an unreviewed safety question. The

licensee did not perform a 50.59 screening of the addition of the jumper until the

QCOP 0300-01 was changed. This licensee identified and corrected violation is being

treattd as a Non-cited Violation (50 254/97014 06; 50-265/1#7014-06) consistent wit i

Section Vll.B.1 of the NRC Enforcement Policy.

Jumoerina Out Alarms for Fire Diesel Pumos

The inspectors reviewed Temporary Alteration Package 97127 written on August 16,

1997, to jumper out the remote alarm capability on the % A and M B diesel driven fire

pumps. The Inspectors identified the 10 CFR 50.59 screening criteria used to ensure an

unreviewed safuy question was not involved mentioned the design requirements of the

remote alarms but did not Odequately justifv their removal. The UFSAR Section 9.5.1.2.0

indicated that standards of tile National Fn Protection Association (NFPA) corte were

followed for fire pump installation. The !.FPA code required both local and remote

annunciation of low oil pressura, high Acket water temperature, failure to start and

overspeed conditions. Temporary A'ioration 97127 failed to discuss these requirements

and why tha removal of the alarm fun:tions did not constitute an unreviewed safety

question. After the inspectors spoke to licensee management, engineers performed a

more thorough review which indicated that an unreviewed safety question was not

involved. Engineering management reviewed this event with engineering personnel.

Ucensee Findinas and Response

The licensee acknowledged weaknesses in adhering to the safety evaluation processes.

Tne licensee identified a wer safety evaluation on a problem associated with the

Unit 2 "C" reactor feed pump. I'his, and other insoector and licensee identified problems

associated with the safety evaluation process, resulted in the Engineering Assurance

Group documenting the process weaknesses on PlF Q1997 3530. The EAG noted some

safety evaluations lacked sufficient information to become quality products. As an interim

musure, engineering required a third party review of all 50.59 reviews in an attempt to

impmvec quality. The licensee was assembling a root cause evaluation team to determine

appropriate corrective actions,

c.

Conclusions

The inspectors concluded engineering processes used to ensure equipment was in

compliance with design requirements were not followed on some occasions. Specifically,

there was no design review for adding a jumper to allow movement of Rod P-4. In

24

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addition, t a Wcial des 1 n review for the fra diesel pump temporary alteration was

9

inadequne. the inspectors concluded engineering and management displayed a poor

understanmg of design change requiremems. Engineering planned third party reviews

as an interim corrective action.

E1.4

Failure to Assure Deslen Basis Recutrements of Safe Shutdown Makeuo Pumo System

a.

Inspection Scone

The inspectors reviewed surveillance test, QCOS 2900-01, Revision 12, "Quarterty Safe

Shutdown Makeup Flow Rate Test,' to assure the test acceptance criteria met

TS requirements and were within the design basi.i of the plant.

The SSMP system was designed as a backup for the reactor core isolation coo'ing

(RCIC) system as part of 10 CFR 50, Appendix R, Section lil.G, " Fire Protection and

Safe Shutdown Capability."

b.

Observations and Findinas

Quad Cities Operational Surveillance 2900-01 acceptance criteria required the

SSMP supply a minimum of 400 gpm, at a minimum pump discharge pressure of

1219.5 psig. This surveillance test was based on original 8 & L calculations which

indicated that with 1219.5 psig at the discharge of the pump and a design flow late of

400 gpm, the system would supply water to the reactor core at the required pressure of

1120 psig. When asked by the inspectors, the licensee could find no documentation that

the tolerances of the installed instrumentation were included into the acceptance criteria

for the pump discharge flow and pressure,

in late July 1996 the system engineer had generated an engineering request,

Engineering Request (ER) 9604270, to address the concem that the discharge pressure

of the safe shutdown makeup pump had degraded and might not be adequate, and

requested a design basis calculation to reconcile instrument accuracy, sensing location,

and plant conditions assumed in the design basis, in September 1996 the SSMP system

was included into the TSs without resolution to ER 9604270. An adequate design basis

calculation was not performed to substantiate the system test acceptance criterta by

taking into r'onsideration instrument accuracy and sensing location. Consequently, the

licensee did not assure the SSMP systera met the TS requirements for system

operability. This was a Violation (50-254/97014-07; 50-265/97014-07) of 10 CFR 50,

Appendix B, Criteria XI, " Test Control' and TS 4.8.J.2.

Following the inspector's identification of this issue, the licensee ran an additional

surveillance test using high accuracy instrumentation. Th!s test verified that the installed

instruraentation was within the tolerance ranges of the high accuracy instruments. The

licensee 6etermined that the acceptance criteria for Unit 1 could not be assured using

only the installed instrumentation. The licensee then declared the SSMP system

inoperable to Unit 1, pl. icing the unit in a 67-day limiting condition for operation (LCO),

while design basis calcelations were verified. The SSMP system to Unit 2 was not

declared inoperable because, due to fewer line losses, the licensd hau a high degree on

confidence that the design basis was met.

25

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c.

canaluelens

.

The licensee failed to act on a system engineer's identification of the unresolved design

basis issues conooming the SSMP system. Consequently, the licensee did not provide

4

i

calculations and validate throug'i testir.g that the TS test acceptance ortteria were met for

SSMP flow and pressure.

E2

Engineering Support of Foollaties and Equipment

.

E2.1

Ooerable but Dearaded Eauloment Lists

a.

Innoodion Sonne (37551)

The inspe::lors reviewed the' licensee's *Open Operability Determinations Log," a Quality

'

and Safety Assessment (QSA) audM and PlFs.

b.

Observations aridfindinns

Due to fouling, icom coolers for the Unit 2 'A' Core Spray Room and "B' Residual H6at

= Removal Room were classified by engineering as " operable but degraded." However, the

inspectors identified that this equipment, and other degraded safety-related equipnient

,

were not included in the "Open Operability Determinations Log" maintained by operations.

This included instalianon of jumpers to remove the alarm functions for both fire diesel

pumps, leakags past the seat for the UnN 2 38 power operated relief valve, a potential

1

condition for the UnN 2 omorgency core cooling system suction strainers to be made of

'

,

improper material, and others. The inspectors spoke to licensee management of these

concoms. The licensee identified that two separate lists of operable, but degraded

'

equip.,iont existed, but were not consistent.

'

The QSA group audited both lists maintained by engineering and operations and

identified the following:

'

three issues on the engineering list were not evaluated for operability corums

seven items on the engineering list which had been reviewed via the PIF proc 6,ss

+

<

had not been evaluated via the operability determination procedure

.

four Mems on the operations list were not on the engineering list

.

eight issues on the operations list newed to be resolved prior to startup from the

+

upcoming planned maintenance outage (Q2P01). Only two of the eight items

were included in the scope of Q2P01.

In Generic Letter g1 18, " Resolution of Degraded and Nonconforreting Conditions," the

NRC lasued guidance on how degraded or nonconforming cond;tions shodd be resolved

commensurate with the safety significance of the issue. The inspectors noted in some

-

instances above, the licensee had not fully evaluated the nature of the degraded

l

condition, and what action wouk' be needed to resolve the condition in a time

,

commensurate with the safety significance.

o

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,

c.

Conduaiana

Lists of important equipment considered operable but degraded were not servlinised well

tr/ either engineering or operations. In some cases, there were no plar,s on when or now

to remove equipmerd from a degraded status. The inspectors concluded the iioensee

displayed a lack of riger in ensuring importard equipment wculd be brought back into

compliance with design requirements within a timely manner.

E2.2

facility Adherence to the Um

While performing the inspections discussed in this report, the inspectors reviewed the

applicable portions of the UFSAR that related to the areas inspected. The inspectors

reviewed plant practices, procedures and/or parameters to that described in the UFSAR

and documented the findings in this inspection report. The inspedors reviewed the

following sections of the UF8AR:

'

IR Section

UFSAR Section

Apolicability

M1.2

8.3.2.1

250 Volt Station Battery

-

-08.3

2.4.4,g.2.5

Ultimate Heat Sink

For the sections reviewed, the inspedors did not identify any discrepancies between plant

configuration and design basis as described in the UFSAR.

E7

Quality Assurance in Engineering Activitica

E7.1

Review of 50.54m Performance Indicator Accountina

a.

Inspection Scope (40500)

By letter dated January 27,1997, the NRC required the licensee to provide additional

information pursuant to 50.54(f) for plans to measure performance improvement at each

Comed nucisar site. - In a response dated March 28,1997, Comed committed to track

each nuciosi station's performance using standard industry indicators on a monthly basis.

The inspectors reviewed three performance indicators reported by the licensee to

corporate. The inspedors reviewed how the licensee complied with the counting

guideline provided by corporate in the desktop instruction manual for three performance

I

inoicators. These performance indicators included temporary alterations, engineering

'

requests (ERs), and ERs overdue,

b.

Observations and Findings

'

l

The inspectors determined the temporary alterations counted at the station and reported

l

to corporate were different. However, the instruction manual allowed for not counting the

following as temporary alterations: ventilation dampers wired open, installation of

- furmanMe clamps, or installation of recorders. After reconciling the reported list with the

-

instructions, the inspedors believed the number of temporary alterations reported offsite

I

- were accurate.

.

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{

The Lg: As determined the method for counting ERs and ERs overdue was not in

!

eewf': .ee with the desktop instruction manual. Spoolfically, ERs counted at the site and

!

i

reported to corpwate did not include parts evaluations and requests for design changes.

!

Similarly, the station only counted 2 of the 19 types of ERs for the ER overdue count.

i

'

The instruction manual required all Priority A and 8 ERs, regardless of ER type, be

.

1

counted.

i

The licensee acknowledged the weakness and admittsd the counting process was still

not consistent between sites. The various sites met to develop a more standardized

,

method of reporting the ER numbers,

i

Section E1.2 of this report documents problems identified by the inspectors where

ER bacidog reduction efforts were not well reviewed, understood or communicated

2

throughout the station.

,

,

i

-

c.

Conclusions

l

"

i

The inspectors concluded some temporary alterations at the site were not included in the

j

count of performance indicatosi. However, the temporary alteration indicator was in

'

compliance with the instructions. The inspectors determined ERs and ERs overdue were

l

not counted in compliance with the !nstructions. The inspectors noted the licensee was

j

attempting to reconcile differences in their counting methodologies to ensure that all sites

were counting the performance indicators consistently. This would allow a better

comparison of performance between Comed sites. The inspectors noted that some

>

efforts to reduce the ER backlog were not reviewed or understood throughout the station.

i

E4

Miscellaneous Engineering issues (92902)

,

' E8.1

(Closed) Unresolved item (URI) 60-254/922&911Q-291/91201-02: This URI had four

'

concams. Concem 2 was no (4ssessment of the effect of higher flows on Unit 1 and Unit

% DGCW pumps and was closed in Inspection Report No. 50 254/92025(DRP);

,

50 265/92025. Concom 3 was the % DGCW pump had not demonstrated meeting the

demands of the M DG Heat Exchanger (HX) and the Unit 1 Emergency Core Cooling

Oystem (ECCS) pump room coolers; and wcs closed in Inspection Report

i

No.50 245/95004(DRP); 50-265/95004(DRP).

l

Concem 4 was an operability question with the Unit 2 DGCW due to unsuccessful flow

'

.

balancing in that most distributions to the individual Unit 2 ECCS room coolers were

L

unknown. The licensee installed flow instrumentation for each of the Unit 2 ECCS room

coolers by Design Change Package (DCP) 9540. The DCP was declared operable on

May 29,1997. The flows were continuously observable and appropriately trended

.

against conservative criteria. Concem 4 is closed.

.

Concem 1 was the Unit 1 DGCW flow was unbalanced and distributions to individual Unit

1 ECCS room coolers were unknown. The differential pressure (D/P) across each Unit 1

ECCS room cooler was well trended by QCOS 5750-9 except during a 7 month period

'

due to an improper engineering tumover (This was considered a Deviation in inspection

Report No.50 254/96010(DRP); 50 265/96010(DRP)). If adverse D/P was detected, the

'

licensee was required to document the condition on a PIF. The licensee would then

inessure flow with a Controlotron Ultrasonic Flowmeter. Any adverse flow detected

i

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a,_

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u -

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>

required an evaluation and the room cooler cleaned if necessary. The licensee was

'

planning on revising QCOS 5750 9 to measure Controlotron flow monthly for t'l Unit 1

ECCS room coolers. Some scaffolding had been installed to facilitate Controlotron

'

measurements. Signi6 card portions of DCP 95 57 had been written to instaN permanent

flow instrumentation for the Unit 1 ECC8 room ooolers and was scheduled for

'

implementation during the UnN 1 Refueling Outage Q1R15 in September of 1998.

!

Concem 1 is closed. This URIis closed.

!

y

E8.2

(Closed) IFl 80 254/93003-01: 50 265/93003-01: The M Diesel Generator Cooling Water

.l

t

Pump Transfer Starter Panel 2251 1H Components Were Not in Preventative

j

Maintenance Progmm. The inspectors vert 6ed the licensee wrote and tracked a

preventive maintenance hem (PM ID 104293) for components on DGCW pump starter

panel 2251 10-0. The electrical maintenance prede6ne coordinator ensured the hem was

!

performed on a 3-year frequency as prescribed by Quad CHies Electrical Maintenance

!

Surveillance (QCEMS) 0250-06, * Exhaust Fan and Room Cool 6r Motor Environmental

!

Quellfloation Surveillance," Revision 7. The panel was specifically delineated in

!

q

Attachmerd F of the procedure, This item is closed.

l

E8.3 (Closed) LER 50 254/94002-00: *B" Control Room Emergency Ventilation (CREV) failure.

,

This LER documented the inoperabilty of the "B" CREV system due to the failure of a

!

4

compressor motor contactor on January 4,1994. The failure of the contactor was

1

'

attributed to cumulative cycling. One cause of the cycling of the contactor was a resuN of

i

the compressor being sized such that it will handle the heat load under extreme

l

conditions. Under normal operating conditions, the compressor frequently cycles as

opposed to running continuously with its load being modulated. A previous cause of

cycling the contactor was the control of cooling water to the condenser which frequently

caused trips / restarts of the compressor resulting in additional cyales of the contactor.

Corrective actions in response to the event included contactor replacement and changes

to operating procedures to bettes control cooling water flow to the condenser. Planned

corrective actions documented in the LER included the insteilation of a hot gas bypass

3

system for the compressor to reduce cycling by inducing a larger heet load on the

'

- compressor to better match its capacity. In the cover letter transmitting the LER to the

NRC, dated January 29,1994, the licensee committod to the NRC to install the

!

l.

  • B" CREV hot gas bypass system. In August 1997 the inspectors reviewed the LER,

l

spoke with engineering staff and determined that the system had not been installed and

!

that design work on the modification had essentially been stopped. The failure to

accomplish this actiot, was a Deviation (50-254/97014-08). This LER is closed.

,

'

E8.4

(Closed) URI 50-254/94004-17: 50-265/9400417: Inoperable Heat Trace Line from Unit

1 Standby Liquid Control (SBLC) Tank to One of the Pumps. The NRC's Diagnostic

.

!

Evaluation Team (DET) identified this condition in September 1993. By November 1993

the licensee had replaced the entire heat tracing system for the SBLC systems for both

units. The replacement systems were improved and have had greater reliability. The

>

minimum low temperature alarm setpoints for both the piping and tanks were increased

!

from 78 to 83* F. The inspectors verified during a walkdown that the new system was in

good material condition with the new controllers indicating 95 ?F. which was their nominal

setpoint. This item is closed.

,

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E8.5

(Closed) URI 50-254/94028-02: 50 265/94028-02: Inadequate Residual Heat Removal

l

Service Water (RHRSW) Surveillance. The inspectors observed that surveillance testing

for the RHRSW room cubicle cooler did not contain limits for acceptable differential

pressure across the cooler. The licensee revised the procedure and established criteria

but concluded that differential pressure measurements alone could not establish

operability of the cooler. The licensee relied on periodic cleaning of the coolers and

differential pressure measurements to assess operability. If differential pressure criteria

,

were not met, engineers measured flow with a portable ultrasonic flowmeter since no flow

,

gauges were installed. Similarly, other required ECCS room coolers did not have

instatied flow gauges. The NRC issued a violation in Inspection Report

No.50 54/97006(DRP); 50 265/97006(DRP) since appropriate corrective action was not

taken in a timely manner to measure flow through the core spray room coolers after

differential pressure measurements exceeded the survelliance procedure acceptance

criteria. This item is closed.

E8.6 (Closed) IFl 50-25E9.5005-03: 50-265/95005-03: Long Term Use of Temporary Sealant

Repair. The inspectors verified that a permanent repair to the leaking 2A recirculation

pump flange was completed during refueling outage Q2R14. This item is closed.

E8.7 (Closed) IFl 50-254/96002-12: 50-265/96002 12: The UFSAR Needed to be Updated to

Reflect the Frequency of a Full Core Off-load and Previous Licensing Commitments. The

licensee revised procedures and updated the UFSAR. Allissues were addressed in the

most recent UFSAR revision annotated Revision 3, December 1995 except for the

clarification conceming storage of other than GE 8x8R fuel. On February 19,1997, a new

nuclear tracking system (NTS) l tem svas opened by the licensee to track this issue. On

September 9,1997, the licensee closed this NTS item. All General Electric fuel critically

analyzes use of one of two methods described in UFSAR section 9.1.2.3. For the

ATRIUM-9B Siemens fuel the licensee will use an analysis as submitted to the

Quad Cities Regulatory Assurance staff on April 23,1997, for incorporation into the

UFSAR. This item is closed.

E8.8 (C.lgytp)_1FI 50-254/9QM2-13: 50-265/96002-13: Problems With Safety-related

.

Control Room Emergency Ventilation (CREV) System. Early in 199C the inspectors noted

numerous equipment problems with the CREV system leading to high unavailability of the

system. The licensee determined the high system unavailability was due to poor work

pisnning and scheduling, several design deficiencies, and a lack of a preventative

mainter,ance program. Subsequent to inspection Report No. 30-254/96002(DRP);

50 265/96002(DRP), in Inspection Report No. 50-254/96017(DRP); 50-265/96017(DRP),

the inspectors documented more design and testing deficiencies with the system. The

NRC lasued two Severity Level IV violations after conducting an enforcement conference

with the licensee. The licenses completed work to restore the system to its original

design basis. The inspectors noted a decreased number of equipment problems since

these efforts were completed. This followup item is closed.

EB.9

(Closed) LER 50-254/96008-00: TS Pressure not Achieved During a Local Leak Rate

Test (LLRT). In response to NRC Information Notica 9613, " Potentia! Containment Leak

Paths Through Hydmgen Analyzers," the licensee identified the containment atmospheric

monitodng inlet piping was not pressurized to 48 pounds per square inch as required by

TS 4.7.A. The licensee determined the cause of the event to be a deficient procedure.

The licensee corrected the procedure.

30

- _ _ _ -

The inspectors determined this was a non-cited violation (50-254/9600815;

50-265/96008 15). The inspectors reviewed the licensees corrective actions. This

LER :s closed.

E8.10 (Closed) Violation 50-265/96010-01: Incorrect Replacement Torus Suction Valve Weight

Used in Safety Evaluation Review. In July 1996 NRC inspectoia were concemed that the

licensee's design review process had failed to identify the consultant's use of the

incorrect valve weight even though no major hazard had been caused. The licensee

conducted an investigation to determine the root cause and any other related conditions.

l

in response to the viol? tion the licensee stated that: (1) even though the documentation

from the consultant indicated to the licensee that the new weight had not been property

taken into consideration, it had been by the actual analysis methodology; (2) some of the

licensee staff had beer, made aware by phone that the correct weight was taken into

consideration but no documentation of the phone call's discussion could be found; (3) the

desl(,n review requirements of Nuclear Engineering Procedure (NEP) 12 03,

  • Nuclear Design I". formation Transmittals (NDITs)," Revision 0, will be more assidcously

enforced in the future; and (4) an engineering department training sess;on to

reemphasize the NDIT design review requirements of NEP 12-03 was held during the

depsrtmental meeting on October 1,1996. The inspectors reviewed the licensee's

followup investigation, and immediate and long-term corrective acitons and found them to

be thorough and acequate. This violation is closed.

E8.11 [Ocen) IFl 50-254/96011-06: 50 265/96011-06: Evaluation of Pipe Whip Impingement

Plate Alteration. While resolving improperlyinstalled concrete expansion anchors

(CEAs), the licensee identified a questionable mounting support for high energy line break

impingement plate 2.JIHP 3. The inspectors reviewed Calculation No. 5061-00 EP 82,

Revision 4, which evaluated this support configuration. After noting that a safety factor of

2.0 was used to qualify the existing CEAs, the inspectors asked the licensee why the

standard safety factor of 4.0 was not used. This was subsequently provided in.

Calculation No. QDC-0000 S 0210, Revision O. After reviewing this information and

discussing it in detail with the licensee, the NRC disagreed with the licensee's technical

arguments justifying their use of the safety factor of 2.0.

The NRC determined that additional analyses and/or anchor bolt capacity upgrades would

be required for high energy pipe whip restraints, in order to meet the CEA manufacturers'

recommended capacities. The NRC staff considered the criteria for CEAs given in

NRC Bulletin 79 02 and in Revision 2 of the Generic Implementation Procedure

developed by the Selcmic Qualification Utility Group for Unresolved Safety Issue A-46 to

be acceptable. Pending a review of the licensee's schedule to complete the additional

analyses or upgrade the anchorage capacity, this item will remain open.

EB.12 LGpsed) LER 50-254/96022 00: "B" CREV System Unable to Maintain 1/8" D/P. The

inspectors verified work was completed to restore the system to its design basis as

described in the UFSAR. Testing conducted on April 22,1997, verified the system could

maintain 1/8" D/P in the control room emergency zone. The inspectors verified that the

licensee submitted to the NRC a revised control room habitability study as committed to

in the corrective actions described in the LER. This LER is closed.

E8.13 (Closed) LER 50 254/97003-00: Missed Visual Examination of High Pressure Coolant

Injection Check Valve. On April 29,1997, the licensee identified a failure to visually

31

_ _ _ _ . _ _ _ _ _ _ _ _

_-

--

examine the Unit 1230145 check valve. As required by the ASME Code for Class 1,2,

and 3 components, the licensee was required to perform a visual examination following

replacement of the valve. The licensee declared the system inoperable until a qualified

inspector examined the valve in accordance with code requirements. The licensee

attributed the missed visual examination to inadequate procedures.

TS 4.0.E required inservice inspection and testing of ASME Code Class 1,2, and 3

components after rt...acement. Failure to perform the required ASME Code visual

inspection constitutes a Violttlon (50 254/97014-01e; 50-265 97014-01e) of TS 4.0.E.

This LER is closed.

IV. Plant Support

R8

Miscellaneous Radiation Protection and Chemistry lasues

R8.1

LQlosed) LER 50-265/97010-00: Missed Chemistry Surveillance. With the Unit 2 *B"

offgas hydrogen analyzer inoperable TS Table 3.2.H 1 required a grab sample of an 8-

hour frequency. On August 19,1997, chemistry technicians missed taking an 8-hour grab

sample from the Unit 2 offgas system. This event was due to a human error. The

licensee counseled the individual. The failure to take the TS required grab sample from

the offgas system was cunsidered a Violation (50-254/97014-01f; 50 265/97014-01f) of

TS 3.2.H. This LER is closed.

F1

Control of Fire Protection Activities

.

The inspectors reviewed several activities related to fire protection and safe shutdown

components, and the related operational maintenance, and engineering activities involved

with supporting these components. Problems with inoperable fire pumps, inoperable safe

shutdown paths, inoperable sprinkler systems, poor tracking of actions needed to track

degraded components, and poor engineering reviews all led to an overall weak

performance in fire protection activities. Some response to safe shutdown p:tblems

discovered by the licensee were considered good.

F1.1

Problems Associated with the "A" Fire Diesel Pumo

a.

Inspection Scooe

The inspectors observed maintenance, testing and troubleshooting activities associated

with the % A diesel fire pump.

b.

Observations and Findinal

After performing annual maintenance to the % A fire diesel pump, the licensee tested the

pump in accordance with QCMMS 4100-32, *% A Diesel Driven Fire Pump Annual

Capacity Test." Having been informed by an insurance representative that alarm testing

for the diesel driven fire pumps was inadequate at Quad Cities because initiation of the

alarm at the sensor was not performed, the licensee corrected the procedure to include

initiation at the sensor (for low oil pressure and high Jacket water temperature). When

testing the alarms with initiation at the sensor, it was discovered that the alarm circuitry

32

L

.

- - _ _ _ _ _

.

._

_ . _ _ _ _ _ . _ _ _ . _ . _ _ . _ _ _

_ _ _ _ _ _

- caused the M A diesel to trip on overspeed. A review of the troubleshooting and repair-

offorts is discussed below. A near miss personnel safety issue occurred during the

testing and is documer6d in sodion M1.3.

Troubleshootina Efforts

Troubleshooting activihes were initially poor. Some of the problems included:

A troublemhooting plan which was expected by the maintenance supenntendent,

was not used. A roct cause evaluation process was not used for several days of

the activity.

The inspectors noted that maintenance history indicated a number of similar

+

failures on both the M A and M B fire pumps since 1993. The root cause for

'

these failures had not been determined in many cases, and trending of the -

problem was not readily available. Maintenance rule evaluations were not

adequate to justify that the failures were not to be considered maintenance rule

j

functional failurer. Resolution of this asp"d is being reviewed in the maintenance

rule inspection (see inspection Report No. 50 254/97017(DRP);-

50 265/97017(DRP)),

!

When initial troubleshooting led technicians to replace the electronk govemor

+

(speed switch), the switch was not adjusted property during instaliation. This

caused the diesel engine to overcrank during subsequent testir g.

Continuity of the repair technicians assigned to the fire pump repair effort was not

]

maintained throughout the troubleshooting process.

i

,

i

The vendor representative brought in to assist in troubleshooting was not certified

+

by the vendor to be qualified for the fire pump diesel engine.

Troubleshootirg activities continued for several days and resulted in the fire pump

i

- exceeding the 7-day administrative LCO time limit. The licensee documented this

condition on a PlF (97-3214).

After 3 days, the license put together a team and a comprehensive troubleshooting plan

to evaluate the root cause of the engine tripping. Possible failure modes were

systematically eliminated. The licensee determined that the cause of the problem was

poor instal!ation of a design modification in 1993 which replaced the mechanical govemor

with an electronic govemor. During installation, wires carrying relatively large alarm bell

currents were routed near wiring transmitting the sensitive electronic govemor speed

signal. The inductive current related to the clearing of the alarm circuit had apparently

caused the r.eart>y unshielded speed sensor circuit to sense overspeed conditions,

causing an overspeed trip. The licensee corrected the trippinn problem by jumpering out

'

the associated alarms.

The inspectors found that the licensee performed a poor review of the desig.1 basis

'

justification for jumpering the alarms (Section E1.3), and. Operations did not property

address operator action required for conditions when the diesel fire pump alarms were

inoperable. Operations had included actions for operators to attend the fire pumps during

.

,

L

33

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_

u

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.-

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. . - .

.

. . .

. - .

-

.~

.

_

_

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_

_

_

'

weekly surveillance operation, but had failed to adequately address actions needed

during emergency fire pump operation and during some auto stPrt conditions. Following

discussions with Operations management, the inspectors verified that the licensee

addressed these concoms with updated surveillance (QCOS 4100 series) and operating

(QCOP 4100 series) procedures .

c.

Conclusion

The inspectors found that poor initial troubleshooting efforts and other maintenance

problems such as improper govemor installation delayed the completion of fire pump

work within the administrative LCO time limits. Later troubleshooting resulted in

discovery of a long standing problem with the fire pump. Justification forjumpering out

fire pump alarms was poor, and operator compensatory actions were not adequately

spelled out.

F1.2

Safe Shutdown Paths Inoperable

a.

Inspection Scop _t

The inspectors reviewed licensee actions upon discovery that 9 of 16 safe shutdown

paths were inoperable,

b.

Observations and Findinas

On August 26,1997, the licensee discovered that proccdures written to support taking

the units to cold shutdown conditions in the event of a fire did not support the

requirements of the fire protection report. This condition rendered 9 of 16 safe shutdown

paths inoperable because tripping of non safe shutdown path loads would not have been

accomplished. The liceasee estimated that the instantaneous fire risk associated with

having nine safe shutdown paths and % A pump inoperable during dual unit operation

would have been approximately 2.7E-03 per reactor year. The licenses took quick action

to correct the procedure discrepancies, began an investigation of the cause of the

discrepancies, and reported the condition on LER 50-254/97021. Previous procedure

problems had been identified in earlier LER reviews, and will be looked at as part of the

review of this LER. Review of this item will be accomplished following the licensee's

review, and tracked as part of followup to the LER.

c.

Conclusions

The inspectors noted that the already relatively high risk associated with fires at

Quad Cities was made even higher by procedure discrepancies in 9 of 1S safe shutdown

paths. Licensee action upon discovery was good, but previous corrective actions for

other LERs and subsequent corrective actions must still be evaluated.

34

'

.

-

. . .

-

F1.3

Poor Corrective Action for Fire Protection Problems

f

a.

Insoection Scope

1

The inspectors observed licensee corrective action for several fire protection issues,

j

including management meetings, action plans for equipment repair, and observation of

compensatory actions in place.

i

b.

Observations and Findinos

The inspectors found operators and managernent to be insensitive to inoperable

fire-related protection equipment problems. Some of this insensitivity appeared to be in

part to a history of equ'pment exceeding administrative LCO times at Quad Cities.

Fire Pumo Dearadation Corrective Action

Since June 27,1994, fire impairment FM-94-152 had been inoperable due to hydraulic

concems with the wet pipe suppression system in the Unit i heater bay. This system has

a 14-day limiting condition for operation action statement which was controlled

administratively (fire protection requirements were removed from Quad Cities TS). On

January 13,1995, fire impairment FM94152 was transferred to FM-95-23. Two other

impairments wero addr.6 on January 1.' "o95, due to hydraulic concems with wet pipe

systems in the Unit 2 heater bay and b .41 Southeast Residual Heat Removal comer

room. Although the LCO time was 14 days, these impairments we~ in effect for over 3

years in some cases without resolution, using fire watches as compensatory actions.

Quad Cities Administrative Procedure (QCAP) 1500-1 * Administrative Requirements for

Fire Protection," only required a non-reportable PIF to be generated when the 14 day LCO

time limit was exceeded.

The hydraulic concems were due to degraded performance of the stations' two diesel

driven fire pumps. The licensee had informed the inspectors on several previous

occasions that a modification was planned and approved to correct these problems with

degraded fire pump performance and to correct problems with zebra mussel blockage of

the fire pump suctions. (Modification number DCP 9600045 was approved for work on

September 24,1996.) The inspectors were informed during this inspection period that

the approved modification had been put on hold due to funding concems. Although

knowing about the funding concems since June 1997, the licensee had no plans in place

for improving fire pump performance and/or correcting the hydraulic impairments. The

inspectors also found that during the recent % A and B fire pump testing, additional

degradation of fire pump flow was noted. In total, a degradation of about 6 percent was

noted since the fire pumps were rebuilt in the 1993 time frame. While this only

exacerbated the original hydraulic impairment problems and did not cause any additional

systems to be inoperable, it did point to the continuing need for effective corrective action

for fire pump problems.

Poor Heater Bay S.prinkler Corrective Actions

On September 8 the inspectors questioned the unit supervisor for Unit 1 about a log entry

mgarding an inoperable sprinkler in the Unit 1 heater bay. The unit supervisor informed

the inspectors that on September 6 a sprinkler head in the heater bay wet pipe system

35

began flooding the heater bay, requiring operators to isolate the entire wet pipe system

for half of the heater bay. When asked about compensatory actions for the isolation of

the wet pipe systern, the unit supervisorindicated that the system was the same system

already in a hng term impairment (since June 1994) and no additional corrective action

other than the fire watches for the original impairment were required.

The inspectors were concemed because the originalimpairment required fire watches

due to a degraded flow condition (about 5 gpm degradation from required flow.) The

problem resolution on September 6 caused the suppression system to have zero flow.

No effective plan for short term maintenance corrective action had been identifieri until

after September 10 following inspectors discussions of the problem with senior station

management. The original plan developed then focused on waiting until hydrogen

injection was scheduled to be tumed off on September 17 (for dose minimization

concems), or 12 days into the period of the isolated wet pipe system. The inspectors

asked station management why the priority was so low that either hydrogen injection

could not be tumed down earlier or reactor power could not be reduced to minimize dose

and complete the work earlier. In the discussion, inspectors pointed out that hydrogen

injection was being tumed off daily on Unit 2 due /o equipment problems. Eventually the

licensee corrected the problem on about September 15, after reducing reactor power to

repair another component.

During the time the wet pipe was isolated, the inspectors observed the fire watches in

place as compensatory meosure. The inspectors noticed on September 9 that cameras

in place for fire watches to monitor were not functioning, and had been noted as needing

repairs for several days. The inspectors notified the operations manager, who later called

for an investigation. The licensee found that several cameras were not providing the

picture adequately for the required fire watches, and documented this on

PlFs Q1997-03450,03437, and 03445. The condidons were corrected and fire watches

were briefed on the proper cameras to watch and what to do in the event of inoperable

cameras. Quad Cities Administrative Procedure 1500-01, Revision 6 dated February 17,

1997, Step D.2.c.2.(b) required a roving (15 mincte) fire watch be estab%hed if a water

suppression system which protects a safe shutdown system is inoperable and the

affected unit is not in a safe shutdown condition. Since the cameras which were

supporting ths hourty fire watch rounds were not fully operable, the NRC and licensee

considered this a case of missed fire watch rounds, a violation of station proc 6dures and

l

ls a Violation (50 254/97014-09; 50-265/97014 09) of TS 6.BA. Generation of a PlF was

l

the only requirement in the QCAP 1500-1 procedure for a missed fire watch and for most

missed fire protection LCOs. The PlF process appeared to be a weak vehicle to focus

station attention on risk important equ;pment and processes. The PlFs reviewed by the

inspectors were given the lowest level in significance and did not generate a higher level

review, even when LCOs were missed by long periods or when multiple systems were

inooerable.

The inspectors found that, in general, fire protection issues received relatively low priority

at Quad Cities, even when exceeding LCO times were involved. Even significant fire

protection LCOs (such as loss of water to the heater bay suppression system) did not

(

receive any significant plan of the day attention or management discussion during

l

meetings observed by the inspectors, compared to balance of plant equipment which

affected generation capability (such as gland seal level control valves.)

.

36

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c.

Conclusion

The inspectors noted an overalllack of sensitivity to fire protection issues. A number of

equipmont problems resulted in administrative LCO time limits being exceeded. Some

equipment was inoperable in excess of 3 years, with planned modifications to repair the

problems recently canceled or changed. This led str'. ion personnel to be less than

aggressive in addressing new fire protection probier.is. Fire watches were the required

compensatory actions for some of these impairments. The inspectors noted a lack of

rigor in ussuring the required fire watches were met, and a violation was cited. Problem

identification forms were not effective in focusing management attention on the fire

protection problems. This all occurred in an environment where the licensee was aware

of a relatively high fire risk at the station.

V. Manaoement Meetinas

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management at the

conclusion of the inspection on September 19,1997. The licensee acknowledged the findings

presented. The inspectors asked the licdases whether any materials examined during the

inspection should be considered proprietary. No proprietary information was identirsed.

.

37

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PARTIAL UST OF PERSONS CONTACTED

!

Lh190199

W. Pearce, She Vice President

'

R. Fairbank. Engineering Manager

F. Famulari, Quality and Safety Assessment

C. Norton, operations Supervisor

C. Peterson, Regulatory Affairs Manager

G. Powell, Radiation Protection Supervisor

M. Weyland, Maintenance Manager

,

t

38

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_

INSPECTION PROCEDURES USED

iP 37551:

Onsite. Engineering

IP 40500:

Effectiveness of Licensee Controls in Identifying, Resolving, and Preventing

Problems

IP 6' 726:

Surveillance Observations

IP 62707:

Maintenance Observations

l

IP 71707:

Plant Operations

IP 92700:

Onsite Followup of Written Reports of Nontouthe Events at Power Reactor

l

Facliities

IP 92701:

Followup Planned Non-Routine Activities

IP 92902:

Followup Engineering

ITEMS OPENED, CLOSED, AND DISCUSSED

Opene.d

50 254/97014 01a; 50-265/97014 01a

VIO

surveillance requirements not met during

50-254/97014-01b; 50-265/97014 01b

rnactor modes

50-254/97014-01c; 50 265/97014-01c

50-254/97014-01d; 50 265/97014 01d

50 254/97014 01e; 50 265/97014-01e

50-254/97014-01f; 50 265/97014 01f

50-265/97014 02

VIO

failure to follow procedure QCMM 1515-07

50-254/97014-03; 50 265/97014-03

NCV discrepancy in QOM check list

50-254/97014-04; 50-265/97014 04

VIO

errors in OCTS 0240-06 resulted in

performance test not being performed

per TS 4.9.5

50 254/97014-05a; 50 265/97014-05a

VIO

design basis information not correctly

50-254/97014 05b; 50-265/97014 05b

translated

50-254/97014 06; 50-265/97014-06

NCV 50.59 screening of the addition of the jumper

not performed until QCOP 0300-01 was

changed

50-254/07014-07; 50-265/97014 07

VIO

no demonstration that SSMP would perform

in accordance with requirements of

TS 4.8.J.2

50-254/97014 08

DEV hot gas bypass system not installed

50-254/97014-09; 50-265/97014-09

VIO

poor heater bay sorinkler corrective actions

Closed

50-254/94010-00

LER

unplanned scram of control rod during

surveillance

50-254/04010-01

LER

unplanned scram of control rod during

surveillance

50-254/96001 00

LER

the *B' CRVS inoperable due to inoperable

relay

50 254/96002-03; 50-265/96002 03

IFl

buildup of debris on trash rack resulted in

low water level inside intake structure

50-254/96006-00

LER

the TS 3.0.A incorrectly 8nvoked

39

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50-254/97001 00

LER

missed operations surveillances

50 254/97008-00

LER

inadequate operations surveillance

50-265/97008-00

LER

missed control rod surveillance

50-265/97009-00

LER

control room operators misread abnormal

offgas radiation readings

50-254/96018-00

LER

misinterpreted TS surveillance requirement

50 254/96018-01

LER

misinterpreted TS surveillance requirement

50 254/97000-05; 50-265/97006-05

IFl

The HPCI suction path transfer from the

CCST to the suppression pool and any

cycling of HPCI on and off considered in the

load profile and modified performance test of

u. ' t 2 250 Vdc battery

50-254/97014 00

LER

the TRSRV did not receive as found set

point testing within 12 mo'1ths

50-254/97016-00

LER

diesel generator cooling water inservice

testing requirements not completed

50-254/92201 02; 50-265/92201 02

URI

no assessment of effect of higher flows on

Unit 1 and Unit % DGCW pumps

50-254/93003 01; 50-265/93003-01

IFl

the % DGCWP transfer starter

panel 2251 10-0 components were not in

preventative maintenance program

50 254/94002-00

LER

this LER documented the inoperability of the

  • B' CREV system due to the failure of a

compressor motor contractor on January 4,

1994

50 254/94004 17; 50-265/94004 17

URI

inoperable heat trace line from Unit i SBLC

tank to one of the pumps

50-254/94028-02;50 265/94028-02

URI

inadequate RHRSW surveillance

50 254/95005-03; 50-265-95005-03

IFl

long term use of temporary sealant repair

50 254/96002 12;50 265/06002 12

IFl

the UFSAR needed to be updated to reflect

the frequency of a full core off load and

previous licensing commitments

50 254/96002-13; 50-265/96002 13

IFl

problems with safety-related CREV system

50-254/96008-00

LER

Technical Specification pressure not

achieved during a LLRT

50-265/96010-01

VIO

incorrect replacement torus suction valve

weight used in safety evaluation review

50-254/96022 00

LER

the "B" CREV system unable to maintain

1/8" D/P

50-254/97003-00

LER

missed visual examination of HPCI check

valve

50 265/97010-00

LER

missed chemistry surveillance

50-254/97014 03; 50-265/97014-03

NCV discrepancy in the QOM check list

50-254/97014-06; 50-265/97014-06

NCV 50.59 screening of the addition of the jumper

not performed until QCOP 0300-01 was

changed

Discussed

50-254/96011-06; 50-265/96011 06

IFl

evaluation of pipe whip impingement plate

alteration

40

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LIST OF ACRONYMS AND INITIALISMS USED

ALARA

As Low As ReasonsHy Achievable

ANSI

American National Standards Institute

ASME

American Suclety of Mechanical Engineers

CCST

Contaminated Coodcasate Storage Tank

CEA

Concrete Expansion Anchors

CFR

Code of Federcl Regulations

Comed

Commonwealth Ecson Company

CRD

Control Rod Drive

CREV

Control Room Emergency Ventilation

d:

direct current

DCP

Design Change f ackage

DET

Diagnostic Evaluation Team

DEV

Deviation

DGCW

Diessi Generator Cooling Water

D/P

Differential Pressure

EAG

Engineering Assurance Group

ECCS

EmergeE:y Core Cooling System

EDG

Emergency Diesel Generator

ELMS

Electrical Load M tnitoring System

ENS

Emergency Notifi:ation System

EOP

Emergency Oil Pump

ER

Engineering Request

GL

Generic Letter

GSC

Gland Steam Condenser

HPCI

High Pressure Coolant injection System

HX

Heat Exchanger

IDNS

lilinois Department af Nuclear Safd *

IEEE

Institute of Electronics of Electricai .ngineers

IFl

Inspector Followup item

IST

Inservice Test

kV

Kilovolt

LCO

Limiting Condition for Operation

LCV

Level Control Valve

iFR

Licensee Event Peport

t

l

LLRT

Loca! Leak Rate Test

LPCI

Low Pre 3sure Coolant injection

MSSV

Main Steam Lafety Valve

NCV

Non-cited Violation

NDIT

Nuclear Design Information Transmittal

NEP

Nuclear Engineering Procedure

NFPA

National Fire Protection Association

NTS

Nuclear Tracking System

OWA

Operator Workarounds

P&lD

Piping and Instrument Diagrams

,

l

PDR

Public Document Room

PIF

Pmblem Identification Form

QCAP

Quad Cities Admin;strative Procedure

QCEMS

Quad Cities Electrical Maintenance Surveillance

41

i

.

. _ -

._

_-_._ _ _.___ ._

_ _ _

. . _ _ _ . _ .

. _ . _ _ _ _ _ _

_

_

,

QCEPM

Quad Cities Electrical Preventive Maintenance

QCGP

Quad Cities General Procedure

QCIP

Quad Cities Instrument Procedure

OCMM

Quad Cities Mechanical Maintenance

QCMMS

Quad Cities Mechanical Maintenance Surveillance

QCOA

Quad Cities Operating Abnormal Procedure

QCOP

Quad Cities Operating Procedure

QCOS

Quad Cities Operating Survelilance Procedure

QCTS

Quad Cities Technical Staff Procedure

QGA

Quad Cities General Abnormal Procedure

'

QOM

Quad Cities Operations Manual

QSA

Quality and Safety Assessment

RCIC

Reactor Core Isolation Cooling System

RG

Regulatory Guide

'

RHR

Residual Heat Removal

RHRSW

Residual heat Removal Service Water

S&L

Sargent and Lundy

SBLC

Standby Liquid Control

SSMP

Safe Shutdown Makeup Pump

SSPV

Scram Solenoid Pilot Valve

TRSRV

Target Rock Safety Relief Valve

TS

Technical Specification

TSUP

Technical Specification Upgrade Program

UFSAR

Updated Final Safety Analysis Report

UPS

Uninterruptible Power Supply

URI

Unresolved Itern

Vdc

Volt direct current

WR

Work Requests

42

_

.

.

_

- __ _ . _

_

__

-_

_ . _ _ ,