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Category:DEFICIENCY REPORTS (PER 10CFR50.55E & PART 21)
MONTHYEARML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20236V3121998-07-29029 July 1998 Final Part 21 Rept Re Enterprise DSR-4 & DSRV-4 Edgs.Short Term Instability Was Found During post-installation Testing & Setup as Part of Design mod/post-work Testing Process. Different Methods Were Developed to Correct Problem ML20248A1671998-05-22022 May 1998 Interim Part 21 Re Enterprise DSR-4 & DSRV-4 Emergency diesel.Post-installation Testing Revealed,High Em/Rfi Levels Affected New Controllers,Whereas Original Controllers Were unaffected.Follow-up Will Be Provided No Later than 980731 ML17309A6211997-09-29029 September 1997 Part 21 Rept Re Final Disposition of Masterflow 713 & Embeco 636 Grout Nonconformance Reported by Master Builders,Inc. Licensee Continuing to Monitor shelf-life of Masterflow 713 & Embeco 636 Grouts Produced at Rancho Cucamonga ML20140G4481997-05-0101 May 1997 Part 21 Rept Re Potential Defect in Component of Dsrv & Dsr Enterprise Standby Diesel Generator Sys.Recommends That Springs Be Inspected on Periodic Basis,Such as During Refueling Outages ML20133E8001997-01-0808 January 1997 Deficiency Rept Re Nonconformance Related to Masterflow 713 Grout,Which Master Builders,Inc Has Supplied as Nuclear SR Product to 18 Npps.Cause Unknown.Requests That Listed Info Be Provided to Gain Insight as to Scope & Possible Cause ML20134H3361996-11-0505 November 1996 Part 21 Rept Re Defective Inner Thrust Bearing 1801461-01 Used in PSA 35 Mechanical Shock Arrestor Used as Restraint on Piping Sys for Nuclear Generating Plant.Lot of Defective Parts Located & Isolated to Three Customers ML20115D2001996-07-0909 July 1996 Part 21 Rept Re Mfg Defect of Enterprise DSR-4 & DSRV-4 Edgs,Originally Mfg by Calcon Corp.Amot Control Corp Purchased Calcon Product Line & Maintains Design & Production.Valves Returned to Cooper Energy Svcs on 960131 ML20117G4641996-05-14014 May 1996 Part 21 Rept Re Cooper Bessemer Reciprocating Products,Div of Cooper Cameron Corp,Issued Ltr to Define Utils/Plants Containing Similar Equipment as Supplied on Cooper Bessemer Ksv & Enterprise Dsr EDGs ML18038A8971994-09-0707 September 1994 Part 21 Rept Re Defect in Latching Mechanism of Potter & Brumfield Relay on C&D High Voltage Shut Down Alarm Assembly Printed Circuit Boards.Pull Test on Relay Reset Button Incorporated Into Receiving Insp Procedures ML20059H7721994-01-17017 January 1994 Part 21 Rept Re Virginia Power Notifying Fairbands Morse Via Failure Analysis Rept NESML-Q-058 of Defective Air Start Distributor cam,16104412 ML20059F2631994-01-0707 January 1994 Part 21 Rept Re Air Start Distributor Cam Mfg by Fairbanks Morse.Mfg Suggests That Site Referenced in Encl App I Inspect Air Start Distributor Cam as Soon as Practical ML20058K3841993-12-0909 December 1993 Part 21 Rept Re Potential Defect in Component of Dsrv & Dsr Enterprise Standby DG Sys,Regarding Potential Problem W/ Subcover Assembled Atop Power Head ML20127H2301993-01-15015 January 1993 Part 21 Rept Re Potential Defeat in Component of Dsrv & Dsr Enterprise Standby DG Sys.Starting Air Distributor Housing Assemblies Installed as Replacement Parts at Listed Sites ML20126J5961992-12-31031 December 1992 Part 21 Rept Re Potential Loss of RHR Cooling During Nozzle Dam Removal.Nozzle Dams May Create Trapped Air Column Behind Cold Leg Nozzle Dam.Mod to Nozzle Dams Currently Underway. Ltrs to Affected Utils Encl ML20126B0421992-12-17017 December 1992 Final Part 21 Rept Re Potential Problem W/Steel Cylinder Heads.Initially Reported on 921125.Caused by Inadequate Cast Wall Thickness at 3/4-inch-10 Bolt Hole.Stud at Location Indicated on Encl Sketch Should Be Removed ML20127D1491992-09-0404 September 1992 Part 21 Rept Re Defect in Component of DSRV-16-4 Enterprise Standby DG Sys Jacket Water Pump Shaft.Caused by Incorrect Tapers Machined on Shaft Due to Vendor Mismatching.All Affected Shafts Recalled & Quality Insp Plans Changed ML17289A6971992-06-26026 June 1992 Amend 1 to Part 21 Rept 158 Re gear-wear Induced Failures in engine-driven Jacket Water Pump in DSRV-16-4 Standby DG Sys. Initially Reported on 911029.Grand Gulf Station Observed Wear Characteristics in as Little as 500 Operating Hours ML20094L1271992-03-13013 March 1992 Amend 1 to Part 21 Rept 159 Re Potential Defect in Power Cylinder Liner.Initially Reported on 920115.Caused by Liner/ Block Fit & Localized Matl Microstructure.All Drawings & Specs Revised to Address Matl Design Requirements ML20087D3191992-01-14014 January 1992 Potential Part 21 Rept Re Problems W/Elmwood/Fasco Contactor Carriers Breaking in Contactor Model 30-FO-30. Caused by Distortion/Shrinkage of Molded Phenolic Contactor Carrier.Replacement Contactors Installed ML17223A5941990-03-0909 March 1990 Errata to 900126 Part 21 Rept Re Anchor/Darling Actuators Incorporating Use of Teldyne-Republic four-way Valves.Lists Plants Inadvertently Left Out in Original Rept ML20005G6831990-01-0505 January 1990 Part 21 Rept Re Installation Instructions for Grommet Use Range for Patel Conduit Seal P/N 841206.Conduit Seals in Environ Qualification Applications Inspected for Proper Wire Use Range & Grommets Replaced ML20248E0121989-09-13013 September 1989 Supplemental Part 21 Rept Re Potential Problem W/Six Specific Engine Control Devices in Air Start,Lube Oil, Jacket Water & Crankcase Sys.Initially Reported on 890429. California Controls Co Will Redesign Valve Seating ML20246K7401989-04-26026 April 1989 Part 21 Rept Re Incorrectly Stamped Name Plates on Certain Asco Nuclear Qualified Valves.Vendor Will Contact Each Affected Facility & Furnish Correctly Stamped Plates & in Near Future Discontinue Sale of Rebuild Kits for Valves ML20247P7991989-04-0404 April 1989 Part 21 Rept Re Atmospheric Dump Valves.Cause of Failure Speculative But Result of Piston Ring That Failed to Seal. Resolution to Problem Requires Increasing Pilot Valve Capacity & Reworking of Plug to Enlarge Pilot Flow Area ML20206M4401988-11-21021 November 1988 Deficiency Rept Re Misapplication of Raychem Criteria in Selection of Some Matl Used in Electrical Cable Field Splice Kits.Initially Reported on 880920.Investigation Is in Process.Final Rept Will Be Submitted by 881222 ML20205C9291988-10-18018 October 1988 Part 21 & Deficiency Rept Re Valves Installed Opposite to Direction of Flow,Per 10CFR21 & 50.55 Requirements.Item Being Tracked by MTS EAI B-5115 & Scheduled for Completion 881030 ML20205D6651988-10-18018 October 1988 Part 21 & Deficiency Rept Re Penetration Seals Found Not to Be Watertight.Initially Reported on 880609.Water Leakage Tests Performed on Unit Upper Cable Spreading Room Seals. All Floor Penetration Seal Assemblies Repaired ML20207P0451988-10-0505 October 1988 Part 21 Rept 146 Re Defect in Left Intercooler Inlet Adapter on Standby Diesel Engine Generator.Recommends Utils Inspect Left Intake Manifold Drain as Part of Operating Plan.Addl Info Expected by 881015 ML20155D6471988-09-28028 September 1988 Deficiency Rept Re Valves Installed Opposite to Direction of Flow.Initially Reported on 880629.Final Rept Delayed Until 881020 ML20207J7361988-09-20020 September 1988 Interim Deficiency Rept Re Misapplication of Vendor Criteria in Selection of Some Matl Used in Electrical Cable Field Splice Kits.Initially Reported on 880601.Final Rept Expected Prior to 881123 ML20153E2271988-09-0101 September 1988 Part 21 & Deficiency Rept Re ESF Filtration Unit Bolts. Initially Reported on 880628.Contractor Conducted Training Session for Personnel to Stress Importance of Clarifying Incomplete Drawing Info & Requirements of Bolting Procedure ML20151V1901988-08-16016 August 1988 Deficiency Rept Re non-water Tight Penetration Seals.Test Rig Constructed to Simulate Typical Upper Cable Spreading Room Configuration & Sealants Verified to Provide Waterproof Seal.Next Rept Will Be Submitted by 881020 ML20196L4811988-07-0707 July 1988 Part 21 & Deficiency Rept Re Valves Installed Opposite to Direction of Flow.Initially Reported on 880601.Investigation in Progress to Determine Full Scope of Condition.Final Rept Will Be Submitted by 881001 ML20151A7781988-07-0606 July 1988 Deficiency Rept Re nonwater-tight Penetration Seals. Initially Reported on 880609.Investigation Incomplete.Next Rept Expected by 880818 ML20196C2971988-06-28028 June 1988 Deficiency Rept Re ESF Filtration Bolts.Initially Reported on 880601.Investigation of Root Cause of Condition Ongoing. Final Rept Will Be Submitted by 880901 ML20195D8541988-06-16016 June 1988 Part 21 Rept Re Potentially Reportable Condition Associated W/Dresser Model 7440W Check Valves Supplied W/Flow Direction Arrow Stamped Opposite to Valve Flow.Investigation Being Conducted.Evaluation of Bechtel Western Power Co Ltr Encl ML20154J4101988-05-12012 May 1988 Addendum 1 to Supplemental Part 21 Rept 145 Re Potential Problem w/F-573-156 Pressure Sensor/Lube Oil Trip.Initially Reported on 880429.Addl 1-1/8-inch Diameter W/Deep Counterbone in Pressure Head Added to Activate Valve ML20154A6841988-05-10010 May 1988 Deficiency Rept Re Electrical Cable Tray Separation. Initially Reported on 880414.Walkdown of All safety-related Cable Trays Conducted to Ensure Any Unacceptable Separation Distance Identified ML20153B6191988-04-29029 April 1988 Part 21 Rept Re Potential Defect in Component of Dsr or Dsrv Standby Diesel Generators Supplied to Utils.Recommends Return of Subj Components in Onsite Warehouse Storage & Suggests Surveillance of Devices Already Installed ML20151K2621988-04-14014 April 1988 Interim Deficiency & Part 21 Rept Re Control Room Essential HVAC Sys.Initially Reported on 870914.Addl Concern Noted Re Incorrect Assumption in Design Calculation.Corrective Action Beyond Calculation Review Involves Logic Mod ML20151K2371988-04-14014 April 1988 Part 21 & Deficiency Rept Re Damage to Emergency Diesel Generator Jacket Water HX During Flushing.Initially Reported on 860917.HX Repaired & Installed in Unit 2.Thermostatic Valves Being Modified ML20148R6441988-01-27027 January 1988 Part 21 & Deficiency Rept Re Protection of Containment Electrical Penetration Assemblies Fabricated by Conax Buffalo Corp.Initially Reported on 871203.LOCA Could Cause One or More of nonsafety-related Circuits to Short Circuit ML20237E9941987-12-22022 December 1987 Deficiency Rept Re Protection of Containment Electrical Penetration Assemblies (Epa).Initially Reported on 871203. Investigations in Progress.Final Rept Will Be Submitted by 880130 ML20236V2981987-11-19019 November 1987 Deficiency Rept Re Electrical Separation Criteria Specified in Const Spec X3AR01.Initially Reported on 870909.Second Test of Electrical Separation Requirements Very Positive. Final Rept Expected to Be Submitted Prior to 880301 ML20236K1431987-11-0202 November 1987 Interim Part 21 & Deficiency Rept Re Inductive Current Interruptive Capacity of Solid State Protection Sys Motor Driven Relay Contacts.Shunt Suppression Device Will Be Added to Solenoid ML20236J5371987-10-29029 October 1987 Part 21 & Deficiency Rept Re Solid State Protection Sys motor-driven Relay Contacts Inductive Current Interruptive Capacity.Initially Reported on 870110.Hardware Mods to Affected Circuits Planned Prior to Fuel Load ML20239A2111987-09-14014 September 1987 Part 21 & Deficiency Rept Re Design of Control Room Essential (CRE) HVAC Sys.Initially Reported on 870713. Backdraft Dampers Added to Unit 1 CRE HVAC Units & Will Be Added to Unit 2 Commensurate W/Const Schedule ML20237H7741987-08-12012 August 1987 Interim Deficiency Rept Re Emergency HVAC Sys in Control Room.Initially Reported on 870713.Engineering Evaluation in Progress to Determine Potential Impacts of Condition on Plant Safety.Final Rept Will Be Submitted by 870915 ML20216E4721987-05-28028 May 1987 Part 21 Rept 140 Re Potential Defect in Air Pressure Regulators Mfg by Bellofram.Dripwell Gasket May Fail Due to Mismachining of Gasket Seating Surface Causing Loss of Control Air & Starting Air Pressure 1999-04-12
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K4591999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20217K8041999-09-30030 September 1999 Rev 1 to Vegp,Unit 2 Cycle 7 Colr ML20217K7741999-09-30030 September 1999 Rev 1 to Vegp,Unit 1 Cycle 9 Colr ML20216E5061999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Vegp,Units 1 & 2. with ML20210P9841999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20209H1211999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20196F9711999-05-31031 May 1999 Owner Rept for ISI for Vogtle Electric Generating Plant, Unit 1 Eighth Maint/Refueling Outage ML20195G1731999-05-31031 May 1999 Monthly Operating Repts for May 1999 for VEGP Units 1 & 2. with ML20206N2141999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20206A6561999-04-21021 April 1999 Safety Evaluation Authorizing Licensee Re Rev 9 to First 10-year ISI Interval Program Plan & Associated Requests for Relief (RR) 65 from ASME Boiler & Pressure Vessel Code ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20206C2291999-03-31031 March 1999 Revised Monthly Operating Repts for Mar 1999 for Vogtle Electric Generating Plant,Units 1 & 2 ML20205Q8081999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Vegp,Units 1 & 2. with ML20205A9581999-03-31031 March 1999 Rev 0 to VEGP Unit 1 Cycle 9 Colr ML20207K6051999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20209H3951999-02-15015 February 1999 Rev 2 to ISI Program Second 10-Year Interval Vogtle Electric Generating Plant Units 1 & 2 ML20209H4091999-02-15015 February 1999 Rev 1 to ISI Program Second 10-Year Interval Vogtle Electric Generating Plant Units 1 & 2 ML20202H9851999-01-29029 January 1999 Safety Evaluation Accepting Rev 8 to First 10-year Interval Inservice Insp Program & Associated Requests for Relief for Vogtle Electric Generating Plant,Unit 1 ML20199F8041999-01-13013 January 1999 Corrected Pages to VEGP-2 ISI Summary Rept for Spring 1998 Maint/Refueling Outage ML20199E7561998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20198S1781998-12-31031 December 1998 SER Re Second 10-year Interval Inservice Insp Program Plan & Associated Requests for Relief for Southern Nuclear Operating Co,Inc Units 1 & 2 ML20196E5221998-12-0101 December 1998 Rev 8 to ISI-P-014, ISI Program for VEGP-2 ML20198B8571998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20195H2131998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Vogtle Electric Generating Station,Units 1 & 2.With ML20154L5681998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Vegp,Units 1 & 2 ML20151W3681998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Vogtle Electric Generating Plant Units 1 & 2.With ML20154L5721998-08-31031 August 1998 Corrected Page from MOR for Aug 1998 for Vegp,Unit 2 ML20237D2051998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Vogtle Electric Generating Plant Units 1 & 2 ML20236V3121998-07-29029 July 1998 Final Part 21 Rept Re Enterprise DSR-4 & DSRV-4 Edgs.Short Term Instability Was Found During post-installation Testing & Setup as Part of Design mod/post-work Testing Process. Different Methods Were Developed to Correct Problem ML20236P6991998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20236Q3051998-06-30030 June 1998 Owner'S Rept for ISI for Sixth Maint/Refueling Outage of Vogtle Electric Generating Plant,Unit 2 ML20249A3911998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Vogtle Electric Generating Plant ML20248A1671998-05-22022 May 1998 Interim Part 21 Re Enterprise DSR-4 & DSRV-4 Emergency diesel.Post-installation Testing Revealed,High Em/Rfi Levels Affected New Controllers,Whereas Original Controllers Were unaffected.Follow-up Will Be Provided No Later than 980731 ML20249A3931998-04-30030 April 1998 Revised MOR for Apr 1998 for Vogtle Electric Generating Plant Unit 1 ML20247F3841998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20154Q9721998-04-20020 April 1998 10CFR50.59(B) Rept of Facility Changes,Tests & Experiments for Vogtle Electric Generating Plant,Units 1 & 2 ML20217H7181998-04-0101 April 1998 Corrected Page 5 to 980324 SER Re Relief Requests Associated W/Second 10-year Interval Insp program.RR-21 in Error in That Component,Suction Damper Inadvertently Omitted. Corrected Page 7 of Technical Ltr Rept Also Encl ML20216D6141998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20217Q1301998-03-31031 March 1998 Rev 0 to Vepc Unit 2 Cycle 7,COLR ML20217B8831998-03-24024 March 1998 SER Accepting Relief Request RR-5,RR-19,RR-20,RR-21,RR-23 & RR-24 for Second 10-yr Interval ISI Program Plan ML20216E2421998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20203H9551998-02-23023 February 1998 SER Denying Quality Assurance Program Description Change for Vogtle Electric Generating Plant,Units 1 & 2 ML20203E4831998-02-11011 February 1998 Rev 1 to Vogtle Electric Generating Plant,Units 1 & 2 Second Ten-Yr Interval Pump Inservice Test Program ML20198T1211998-01-31031 January 1998 Owners Rept for Inservice Inspection for Seventh Maintenance/Refueling Outage ML20202G5441998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20199E5431998-01-31031 January 1998 Rev 3 to WCAP-14720, Vogtle Units 1 & 2 Spent Fuel Rack Criticality Analysis W/Credit for Soluble Boron ML20198L6471997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Vogtle Electric Generating Plant,Units 1 & 2 ML20203C2811997-12-0909 December 1997 Safety Evaluation Authorizing Request for Relief of Second 10 Yr Interval Inservice Insp Program ML20202B7881997-12-0101 December 1997 Rev 8 to ISI-P-006, ISI Program for Gpc Vogtle Electric Generating Plant Unit 1 ML20203H0601997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Vegp,Units 1 & 2 1999-09-30
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o w Georgia Power Company Route 2. Box 299A Waynesboro Georgia 30830 Telephone 404 554 996t. Ext 3360 404 724-8114. Ext. 3360 L
o.o.rou., Oo EC20 AfD : 2 6 Georgia Power Vice President and Project General Manager tne southem e:ectoc system Vogtie Project August 15, 1985 United States Nuclear Regulatory Comrrission File: X78G03-M75 Office of Inspection and Enforcement Log: GN-683 Region II-Suite 2900 101 Marietta Street, Northwest Atlanta, Georgia 30323
Reference:
Vogtle Electric Generating Plant-Units 1 & 2, 50-424, 50-425; Jumper and Jumper Package Controls Letter GN-617, dated May 17, 1985 Attention: Mr. J. Nelson Grace In previous correspondence to the NRC on this subject, Georgia Power Company indicated that we expected to notify the NRC of the results of our evalaution of the above referenced subject on or before August 16, 1985. Georgia Power Company has concluded its evaluation and determined that a reportable condition per the criteria of part 10CFR50.55(e) did exist. Our evaluation also concluded that a reportable condition per Part 10CFR21 did not exist. Enclosed is a copy of our evaluation. '
This response contains no proprietary information and may be placed in the NRC Public Document Room.
4 Ve y truly rs,
%8 $$N $50$
{ D. O. Foster REF/D0F/wkl xc: U. S. Nuclear Regulatory Commission Document Control Desk 6~ Washington, D.C. 20555 R. J. Kelly J. A. Bailey G. Bockhold R. E. Conway 0. Batum P. D. Rice G. F. Head H. H. Gregory C. S. McCall J. T. Beckham W. T. Nickerson E. L. Blake, Jr.
R. A. Thomas D. R. Altman (Shaw, et. al'. )
D. E. Dutton D. L. Kinnsch (BPC) J. E. Joiner W. F. Sanders (NRC) J. L. Vota (W) (Troutman, et. al.
R. H. Pinson L. T. Gucwa D. C. Teper (GANE) )
B. M. Guthrie C. E. Belflower L. Fowler (LEAF) gg ,
E. D. Groover F. B. Marsh (BPC) T. Johnson (ECPG)
R. W. McManus G. A. McCarley g
4 EVALUATION FOR A POTENTIAL REPORTABLE CONDITION Jumper and Jumper Package Control Initial Report-On April 19, 1985, Mr. C. W. Hayes, Vogtle Project Quality Assurance Manager, informed Mr. M. Sinkule of the USNRC of a potential reportable condition involving jumper and jumper package control ar.d the interr al wiring of equipment. In a subsequent letter to the NRC, Georgia Power Company indicated that a final response could be expected on or before August 16, 1985.
Background Information:
Georgia Power Company conducted a special electrical assessment audit to verify the adequacy and implementation of requirements and controls established for the Vogtle electrical activities. This audit identified concerns associated with the control of jumpers and jumper packages and with the internal wiring of equipment. Several instances were noted of incorrect jumper installations. These included a jumper landed to an incorrect terminal, jumpers not installed, and juiaper location incorrect as specified by engineering. Additionally, it appears that the Main Control Board termination cabinets had been wired incorrectly.
It should be noted that jumper packages are orginated "by equipmcat" when they are turned over with a subsystem. When an instruinent cabinet has a jumper package that is initially prepared, all electrical drawings will be reviewed and c jumper package will be prepared for the cabinet.
This package will give the electrical installer detailed instructions for the internal wiring within the cabinet. This system is corrpletely tanual and mandates a tedious review when ascertaining the status of jumper in a specific application. Jumpers that are not installed per the design drawing could cause circuits to be inoperable and therefore, prevent the performance of a safety related function. Additionally, a review of the main control board termination cabinets revealed that the electrical contractor for the Vogtle Project, Clevelar.d Electric, had inadvertantly switched approximately six termination racks.
It should be noted that both of these concerns were detected by the
" red-lining" process. The Nuclear Operations group of Georgia Power Company has been red-lining all safety-related electrical circuits.
In this process, every circuit is checked to ensure that the electrical connections are properly connected.
Engineering Evalution:
Bechtel Power Corporation has ccnducted an engineering evaulation of this cordition. This evaluation found incorrect ~iy wired jumpers tnat could have, if uncorrected, prevented the performance of safety-related functions.
. . o D
In one case, a jumper wire was not installed as talled for by the drawing. This condition could have prevented a damper from opening when the train A motor is running. As a result, the following could have occurred:
A) The HVAC system upstream of this damper is for clean-up leveis of the A, B, C and D piping penetration rooms. Normal emergency design operation for tnis equipment would require the damper to be opened in order to return approximately 90 percent of the filtered air to these spaces. The remaining percentage is exhausted to the stack. With the damper fully closed, all of the filtered air is discharged to the plant vent. '4hile the fan is operating, the discharge radiation limits would not i>e exceeded since all exhaust air is filtered prior to discharge.
B) With the damper closed, the fan would "back up" on the fan curve and would eventually shutdown due to low flow or excessive vibration.
Shutdown of this filtration train would not result in exceeding environmental qualification temperatures since each room, where safety related equipment is located, is equipped with individual room cubicle coolers which act independently of the filtration train. Shutdour, of the fan would, however, result in the loss of negative pressure in the individual rooms and the migration of radioactivity through the walls and openings and ultimately to the environment, thereby possibly exceeding the maximum allowable radiation dose limits. (10CFR50 Appendix A, GDC 19)
In another case, a missing jumper wire would have prevented the B train of the control building eletrical penetration filter unit from operating.
The control building filter exhaust system is designed to minimize the release of airborne radioactivity to the outside atmosphere by processing recirculated and exhaust air through carbon filters. This system is part of the engineered safety features (ESF) provided for the building. An assumed single failure of the A train could result under postulated accident conditions, in a spread of radioactivity in the control building.
The audit also identified that equipment internal wiring was not in compliance with vendor rirawings. In this case, it was discovered that terminal boards of the Unit 1 main control board termination cabinets were interchanged. The interchanging of the terminal board would result in a failure of the main control board to function properly. The switching of the terminal boards would have been detected during system pre-operational check-out, since none of the affected systems would have properly functioned. The interchanging of the terminal boards occurred in September and October 1983. In November, 1983, procedures were writter. to control material traceability.
E a
Conclusion:
Georgia Power Company has evaluated the conditions described in the engineering evaluation and concluded that a reportable condition per the criteria of Part 10CFR50.55(e) does exist.
Based upon guidance provided by NUREG-0302 Rev. 1, Georgia Power Company has concluded that this condition is not reportable per Part 10CFR21.
Corrective Action:
- 1. Jumper and Jumper Package Controls The corrective action for this condition is essentially complete. These actions included:
Re-training the responsible engineers in the revised procedures and controls for jumper installations.
Assigning an experienced termination engineer into the equipment
- group.
" Jumper packages" are not originated until the Turnover Engineer provides field engineering a list of the equipment in the turnover.
The QA vault and Turnover Engineer are provided a copy of the " jumper package" list.
I Prior to turnover, field engineering and the QA vault verify all l " jumper packages" listed for the turnover are complete and documented.
A computer tracking system es developed and initiated (about 25%
of the data inputed to date) for jumper control.
l The field procedure controlling the preparation, installation, and Quality Control inspections was completely revised, l
- 2. " Equipment / Component Removal," procedure GD-T-28, Revision 0, was l implemented in November,1983. This procedure provided the controls l and documentation necessary to ensure that materials, parts, and components are properly identified and traceable throughout fabrication, erection, and installation of the items. In this sense, it provided the additional measure of control to ensure that equipment partially disassembled during installation or construction was returned to its original condition in a controlled, documented manner prior to use. This procedure supplemented those other procedures which were specific for a particular equipment installation. In its present form, this procedure should prevent the situation from recurring.