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MONTHYEARML20050B5681982-03-31031 March 1982 Advises That Evaluation of NUREG-0737,Item II.D.1 Re Testing of Pressurizer Code Safety & Power Operated Relief Valves Underway.Resolution Available for Required 820701 Submittal Project stage: Request ML20054L1831982-07-0101 July 1982 Responds to NUREG-0737,Item II.D.1 Re Pressurizer Code Safety & Pilot Operated Relief Valve Testing.Util Participated in EPRI Administered Safety & Relief Valve Testing Program.Evaluation to Be Submitted by 821231 Project stage: Other ML20128N8361982-09-30030 September 1982 Performance Test Program for Increased Blowdown on Crosby 4M16 HB-BP-86 Pressurizer Safety Valve Project stage: Other ML20070H7671982-12-17017 December 1982 Advises That Final Evaluation Re EPRI Relief & Safety Valve Testing Per NUREG-0737,Item II.D.1, Reliability Engineering, Will Not Be Submitted Until 830131.Summary of Evaluation Submitted Project stage: Other ML20070T0961983-02-0101 February 1983 Forwards Rev 0 to Davis-Besse Analysis & Evaluation of Safety/Relief Valve Discharge Sys Per NRC NUREG-0737, Technical Rept,In Response to Items II.D.1.2 & II.D.1.3 Project stage: Other ML20028G0701983-02-0202 February 1983 Forwards Response to 821227 Request for Info Re Plant Computer Sys & non-nuclear instrumentation-X Power Failure Project stage: Request ML20128N8071985-07-19019 July 1985 Provides Partial Response to 850607 Request for Addl Info Re NUREG-0737,Item II.D.1 Concerning Selection of Transients & Valve Inlet Conditions,Valve Operability & Analysis of Inlet & Discharge Piping Project stage: Request ML20137Y5621985-10-0101 October 1985 Forwards Response to Question 2 of 850719 Request for Addl Info Re NUREG-0737,Item II.B.1 Concerning Expected Blowdowns at Current Ring Settings.Actual Percent Blowdown of Safety Valves Has No Adverse Effect Upon Core Cooling Project stage: Request ML20138A7731985-12-0606 December 1985 Forwards Partial Response to 850607 Request for Addl Info Re NUREG-0737,Item II.D.1.Safety Valves Removed from Original Location in Valve Room to Direct Mount on Pressurizer Nozzles Project stage: Request 1983-02-01
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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217P2061999-10-26026 October 1999 Forwards for First Energy Nuclear Operating Co Insp Rept 50-346/99-17 on 990928-1001.Insp Was Exam of Activities Conducted Under License Re Implementation of Physical Security Program.No Violations Identified ML20217N3851999-10-20020 October 1999 Forwards RAI Re Licensee 990521 Request for License Amend to Allow Irradiated Fuel to Be Stored in Cask Pit at Davis-Besse,Unit 1.Response Requested within 60 Days from Receipt of Ltr ML20217N2321999-10-15015 October 1999 Requests NRC Approval to Use Alternative to Requirements of 10CFR50.55a(f)(4)(ii).Licensee Requests Extension to Specified Schedule for Implementing Updates to IST Program ML20217G9201999-10-14014 October 1999 Discusses Utils Request for Approval of Quality Assurance Program Changes PY-CEI-NRR-2438, Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl1999-10-14014 October 1999 Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl ML20217F8371999-10-0808 October 1999 Forwards Insp Rept 50-346/99-10 on 990802-0913.One Violation Occurred Being Treated as NCV ML20217A5641999-09-30030 September 1999 Informs of Completion of mid-cycle PPR of Davis-Besse on 990901.Informs That NRC Plans to Conduct Addl Insps to Address Questions Raised by Issues Re Operator Errors & Failure to Commit to JOG Topical Rept on MOV Verification ML20212L0691999-09-30030 September 1999 Forwards,For Review & Comment,Copy of Preliminary ASP Analysis of Operational Condition Discovered at Unit 1 on 981014,as Reported in LER 346/98-011 ML20216J6701999-09-24024 September 1999 Forwards Post Examination Documentation for Written Operator Initial License Examination Administered at Davis-Besse Nuclear Power Station on 990920.Without Encls ML20212D3501999-09-21021 September 1999 Forward Copy of Final Accident Sequence Precursor Analysis of Operational Event at Plant,Unit 1 on 980624,reported in LER 346/98-006 05000346/LER-1998-001, Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached1999-09-0909 September 1999 Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached ML20216E5961999-09-0707 September 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1,safety Features Actuation Sys Instrumentation & Associated Bases 3/4.3.1 & 3/4.3.2,reactor Protection Sys & Safety Sys Instrumentation ML20211P3001999-09-0707 September 1999 Forwards FEMA Transmitting FEMA Evaluation Rept for 990504 Emergency Preparedness Exercise at Davis-Besse Nuclear Power Plant.No Deficiencies Identified.One Area Requiring C/A & Two Planning Issues Identified ML20211K6681999-08-30030 August 1999 Forwards Copies of Certified Personal Qualification Statement - Licensee (NRC Form 398) for Operator Candidates Listed Below.Without Encls ML20211K6611999-08-30030 August 1999 Forwards Copies of Operator License Renewal Applications for Individuals Listed.Operators Have Successfully Completed Appropriate Operator Requalification Training Program at Dbnps.Without Encls ML20211K0951999-08-30030 August 1999 Forwards Request for Addl Info Re Fire & Seismic Analyses of IPEEE for Davis-Besse Nuclear Power Station,Unit 1. Response Requested within 60 Days ML20211H0201999-08-25025 August 1999 Forwards semi-annual FFD Rept for 990101-0630 for DBNPS, Unit 1,IAW 10CFR26.71(d) ML20211D1171999-08-20020 August 1999 Forwards Insp Rept 50-346/99-09 on 990623-0802.Violations Identified & Being Treated as Noncited Violations ML20211G3911999-08-20020 August 1999 Forwards Update to Estimated Info for Licensing Action Requests Through 010930,re Administrative Ltr 99-02, Operating Reactor Licensing Action Estimates PY-CEI-NRR-2411, Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl1999-08-19019 August 1999 Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl ML20211J9201999-08-13013 August 1999 Urges NRC to Find Funds for Stockpiling Radiation Pills for Residents Living Near Plant ML20211B0161999-08-13013 August 1999 Forwards SE Accepting Evaluation of Second 10-year Interval Inservice Insp Program Request for Relief Numbers RR-A16, RR-A17 & RR-B9 for Plant,Unit 1 ML20210T1061999-08-12012 August 1999 Forwards Preliminary NRC Forms 398 & 396 for Listed Candidates,Per Operator License Exam Scheduled for Week of 990913.Encl Withheld ML20210S6071999-08-11011 August 1999 Provides Final Response to NRC RAI Re GL 98-01, Y2K Readiness of Computer Systems at Npps ML20210P8051999-08-0909 August 1999 Forwards Insp Rept 50-346/99-15 on 990712-16.No Violations Noted.However,Several Deficiencies Were Identified with Implementation of Remp,Which Collectively Indicated Need for Improved Oversight of Program IR 05000346/19980211999-08-0606 August 1999 Refers to NRC Insp Rept 50-346/98-21 Conducted on 980901- 990513 & Forwards Nov.Two Violations Identified Involving Failure to Maintain Design of Valve & Inadequate C/A for Degraded Condition Cited in Encl NOV 05000346/LER-1998-009, Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl1999-08-0606 August 1999 Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl ML20210H6101999-07-30030 July 1999 Informs That Region III Received Rev 21 to Various Portions of Davis-Besse Nuclear Power Station Emergency Plan.Revision Was Submitted Under Provisions of 10CFR50.54(q) in Apr 1999 ML20210H0491999-07-28028 July 1999 Forwards Application for Amend to License NPF-3,revising TS 3/4.7.5.1, Ultimate Heat Sink, to Allow Plant Operation in Modes 1-4 with Water Temp Less than or Equal to 90 F ML20210G5521999-07-28028 July 1999 Provides Addl Response to 980923 OL Licensing Exam Rept 50-346/98-301 Re OL Exam Administered in Aug 1998.Results of Root Cause Investigation & Corrective Actions,Discussed ML20210G3831999-07-27027 July 1999 Forwards Application for Amend to NPF-3,changing TSs 6.4, Training, 6.5.2.8, Audits, 6.10, Record Retention, 6.14, Process Control Program & 6.15, Odcm ML20211P3071999-07-26026 July 1999 Forwards Final Rept for 990504 Biennial Radiological Emergency Preparedness Exercise for David-Besse Power Station.No Deficiencies Identified for Any Jurisdiction During Exercise ML20210G4391999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1, Safety Features Actuation Sys Instrumentation, & Associated Bases 3/4.3.1 & 3/4.3.2, Reactor Protection Sys & Safety Sys Instrumentation ML20210G7151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising TSs 3/4.3.3.1, Radiation Monitoring Instrumentation, 3/4.3.3.2, Instrument - Incore Detectors & 3/4.3.3.9, Instrumentation - Waste Gas Sys Oxygen Monitor ML20210G5151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs for Implementation of 10CFR50,App J,Option B for Type B & C Containment Leakage Rate Testing ML20210G3211999-07-26026 July 1999 Forwards Written OL Exam & Supporting Matl for Exam to Be Administered at DBNPS During Week of 990913.Listed Encls Withheld from Public Disclosure Until After Exam Complete ML20210C4381999-07-20020 July 1999 Forwards Insp Rept 50-346/99-08 on 990513-0622.Unidentified RCS Leak Approached TS Limit of 1 Gallon Per Minute Prior to Recently Completed Maint Outage.Three Violations of NRC Requirements Identified & Being Treated as NCVs ML20209G3681999-07-15015 July 1999 Advises That Info Submitted in & 990519 Affidavit Re Design & Licensing Rept,Davis-Besse,Unit 1 Cask Pit Rack Installation Project,Holtec Intl, HI-981933,marked Proprietary,Will Be Withheld from Public Disclosure ML20207H6401999-07-0909 July 1999 Discusses Closure of TAC MA0540 Re Util Responses to RAI on GL 92-01,rev 1,suppl 1, Rv Structural Integrity. Staff Has Revised Info in Rvid & Releasing It as Rvid Version 2 ML20209D1341999-07-0808 July 1999 Forwards Notice of Withdrawal of Application for Amend to Operating License.Proposed Change Would Have Modified Facility TSs Pertaining to Allowable as-found Pressure Lift Setting Tolerance of Two Pressurizer Code Safety Valves 05000346/LER-1998-012, Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached1999-07-0707 July 1999 Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached ML20209C3981999-07-0101 July 1999 Responds to NRC Re Violations Noted in Insp Rept 50-346/98-21.Corrective Actions:Developed Rev to Boric Acid Control Program & Work Process Guideline on Plant Leakage ML20209B5821999-06-24024 June 1999 Provides Justification for Rev to Completion Date for One of Insp follow-up Items Cited in Insp Rept 50-346/98-03, Designated as Inspector follow-up Item 50-346/97-201-10 ML20196G1251999-06-23023 June 1999 Responds to NRC RAI Re GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20196E5321999-06-17017 June 1999 Forwards Addl Info Re Relief Request RR-A16 to Support NRC Approval of Relief Request ML20195K2751999-06-16016 June 1999 Forwards Safety Evaluation Re GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20196A6601999-06-16016 June 1999 Forwards Master Decommissioning Trust Agreements Revised After 1990 for Ohio Edison Co,Cleveland Electric Illuminating Co,Toledo Edison Co & Pennsylvania Power Co Re Bvnps,Units 1 & 2,DBNPS,Unit 1 & Perry Unit 1 ML20195F9071999-06-10010 June 1999 Forwards Application for Amend to NPF-3,changing Tech Specs 3/4.6.4.4, Hydrogen Purge Sys, TS 3/4.6.5.1, Shield Bldg Emergency Ventilation Sys & TS 3/4.7.6.1, Crevs ML20195F8851999-06-0707 June 1999 Withdraws 950929 License Amend Application,Proposing Mod to Allowable as-found Pressure Lift Setting Tolerance of Two Pressurizer Code Safety Valves ML20207G0751999-06-0707 June 1999 Forwards Insp Rept 50-346/99-04 on 990323-0513.Violations Occurred & Being Treated as non-cited Violations,Consistent with App C of Enforcement Policy 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217N2321999-10-15015 October 1999 Requests NRC Approval to Use Alternative to Requirements of 10CFR50.55a(f)(4)(ii).Licensee Requests Extension to Specified Schedule for Implementing Updates to IST Program PY-CEI-NRR-2438, Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl1999-10-14014 October 1999 Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl ML20216J6701999-09-24024 September 1999 Forwards Post Examination Documentation for Written Operator Initial License Examination Administered at Davis-Besse Nuclear Power Station on 990920.Without Encls 05000346/LER-1998-001, Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached1999-09-0909 September 1999 Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached ML20216E5961999-09-0707 September 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1,safety Features Actuation Sys Instrumentation & Associated Bases 3/4.3.1 & 3/4.3.2,reactor Protection Sys & Safety Sys Instrumentation ML20211K6611999-08-30030 August 1999 Forwards Copies of Operator License Renewal Applications for Individuals Listed.Operators Have Successfully Completed Appropriate Operator Requalification Training Program at Dbnps.Without Encls ML20211K6681999-08-30030 August 1999 Forwards Copies of Certified Personal Qualification Statement - Licensee (NRC Form 398) for Operator Candidates Listed Below.Without Encls ML20211H0201999-08-25025 August 1999 Forwards semi-annual FFD Rept for 990101-0630 for DBNPS, Unit 1,IAW 10CFR26.71(d) ML20211G3911999-08-20020 August 1999 Forwards Update to Estimated Info for Licensing Action Requests Through 010930,re Administrative Ltr 99-02, Operating Reactor Licensing Action Estimates PY-CEI-NRR-2411, Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl1999-08-19019 August 1999 Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl ML20211J9201999-08-13013 August 1999 Urges NRC to Find Funds for Stockpiling Radiation Pills for Residents Living Near Plant ML20210T1061999-08-12012 August 1999 Forwards Preliminary NRC Forms 398 & 396 for Listed Candidates,Per Operator License Exam Scheduled for Week of 990913.Encl Withheld ML20210S6071999-08-11011 August 1999 Provides Final Response to NRC RAI Re GL 98-01, Y2K Readiness of Computer Systems at Npps 05000346/LER-1998-009, Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl1999-08-0606 August 1999 Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl ML20210H0491999-07-28028 July 1999 Forwards Application for Amend to License NPF-3,revising TS 3/4.7.5.1, Ultimate Heat Sink, to Allow Plant Operation in Modes 1-4 with Water Temp Less than or Equal to 90 F ML20210G5521999-07-28028 July 1999 Provides Addl Response to 980923 OL Licensing Exam Rept 50-346/98-301 Re OL Exam Administered in Aug 1998.Results of Root Cause Investigation & Corrective Actions,Discussed ML20210G3831999-07-27027 July 1999 Forwards Application for Amend to NPF-3,changing TSs 6.4, Training, 6.5.2.8, Audits, 6.10, Record Retention, 6.14, Process Control Program & 6.15, Odcm ML20210G7151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising TSs 3/4.3.3.1, Radiation Monitoring Instrumentation, 3/4.3.3.2, Instrument - Incore Detectors & 3/4.3.3.9, Instrumentation - Waste Gas Sys Oxygen Monitor ML20210G5151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs for Implementation of 10CFR50,App J,Option B for Type B & C Containment Leakage Rate Testing ML20210G3211999-07-26026 July 1999 Forwards Written OL Exam & Supporting Matl for Exam to Be Administered at DBNPS During Week of 990913.Listed Encls Withheld from Public Disclosure Until After Exam Complete ML20210G4391999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1, Safety Features Actuation Sys Instrumentation, & Associated Bases 3/4.3.1 & 3/4.3.2, Reactor Protection Sys & Safety Sys Instrumentation ML20211P3071999-07-26026 July 1999 Forwards Final Rept for 990504 Biennial Radiological Emergency Preparedness Exercise for David-Besse Power Station.No Deficiencies Identified for Any Jurisdiction During Exercise 05000346/LER-1998-012, Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached1999-07-0707 July 1999 Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached ML20209C3981999-07-0101 July 1999 Responds to NRC Re Violations Noted in Insp Rept 50-346/98-21.Corrective Actions:Developed Rev to Boric Acid Control Program & Work Process Guideline on Plant Leakage ML20209B5821999-06-24024 June 1999 Provides Justification for Rev to Completion Date for One of Insp follow-up Items Cited in Insp Rept 50-346/98-03, Designated as Inspector follow-up Item 50-346/97-201-10 ML20196G1251999-06-23023 June 1999 Responds to NRC RAI Re GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20196E5321999-06-17017 June 1999 Forwards Addl Info Re Relief Request RR-A16 to Support NRC Approval of Relief Request ML20196A6601999-06-16016 June 1999 Forwards Master Decommissioning Trust Agreements Revised After 1990 for Ohio Edison Co,Cleveland Electric Illuminating Co,Toledo Edison Co & Pennsylvania Power Co Re Bvnps,Units 1 & 2,DBNPS,Unit 1 & Perry Unit 1 ML20195F9071999-06-10010 June 1999 Forwards Application for Amend to NPF-3,changing Tech Specs 3/4.6.4.4, Hydrogen Purge Sys, TS 3/4.6.5.1, Shield Bldg Emergency Ventilation Sys & TS 3/4.7.6.1, Crevs ML20195F8851999-06-0707 June 1999 Withdraws 950929 License Amend Application,Proposing Mod to Allowable as-found Pressure Lift Setting Tolerance of Two Pressurizer Code Safety Valves ML20207F4231999-06-0202 June 1999 Forwards Rev 1 to DBNPS Emergency Preparedness Evaluated Exercise Manual 990504, IAW 10CFR50.4.NRC Evaluated Exercise Has Been Rescheduled for 991208,since NRC Did Not Evaluate 990504 Exercise ML20207E2521999-05-28028 May 1999 Forwards Rev 18,App A,Change 1 to Davis-Besse Nuclear Power Station,Unit 1,industrial Security Plan IAW Provisions of 10CFR50.54(p).Encl Withheld,Per 10CFR73.21 ML20207E9561999-05-28028 May 1999 Forwards Update to NRC AL 98-03,re Estimated Info for Licensing Activities Through Sept 30,2000 ML20207E7801999-05-21021 May 1999 Forwards Application for Amend to License NPF-3,allowing Use of Expanded Spent Fuel Storage Capacity.Proprietary & non- Proprietary Version of Rev 2 to HI-981933 Re Cask Pit Rack Installation Project,Encl.Proprietary Info Withheld ML20206N0231999-05-0606 May 1999 Forwards License Renewal Applications for Davis-Besse Nuclear Power Station,Unit 1 for ML Klein,Cn Steenbergen & CS Strumsky.Without Encls ML20206D2421999-04-28028 April 1999 Forwards Combined Annual Radiological Environ Operating Rept & Radiological Effluent Release Rept for 1998. Rev 11, Change 1 to ODCM & 1998 Radiological Environ Monitoring Program Sample Analysis Results Also Encl PY-CEI-NRR-2382, Forwards 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for FY98 Also Encl1999-04-21021 April 1999 Forwards 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for FY98 Also Encl ML20206B8831999-04-17017 April 1999 Forwards 1634 Repts Re Results of Monitoring Provided to Individuals at Davis-Besse Nuclear Power Station During 1998,per 10CFR20.2206.Without Repts ML20205K3871999-04-0707 April 1999 Forwards Copy of Application of Ceic,Oec,Ppc & Teco to FERC, Proposing to Transfer Jurisdictional Transmission Facilities of Firstenergy Operating Companies to American Transmission Sys,Inc.With One Oversize Drawing ML20205K5641999-04-0707 April 1999 Forwards Response to NRC 980415 RAI Re GL 96-06, Assurance of Equipment Operability & Ci During Design-Basis Accident Conditions. Rept FAI/98-126, Waterhammer Phenomena in Containment Air Cooler Swss, Encl ML20205J1171999-03-29029 March 1999 Forwards Rev 1 to BAW-2325, Response to RAI Re RPV Integrity, Per GL 92-01,Rev 1,Suppl 1, Reactor Vessel Structural Integrity. Rev Includes Corrected Values in Calculations PY-CEI-NRR-2377, Submits Decommissioning Repts for Bvps,Units 1 & 2,Davis- Besse Nuclear Power Station,Unit 1 & Perry Nuclear Power Plant,Unit 1,per 10CFR50.75(f)(1)1999-03-29029 March 1999 Submits Decommissioning Repts for Bvps,Units 1 & 2,Davis- Besse Nuclear Power Station,Unit 1 & Perry Nuclear Power Plant,Unit 1,per 10CFR50.75(f)(1) ML20205F5961999-03-27027 March 1999 Forwards Comments on Preliminary Accident Sequence Percursor (ASP) Analysis of 980624 Operational Event at Dbnps,Unit 1, as Transmitted by NRC Ltr ML20205D4791999-03-26026 March 1999 Forwards Rept Submitting Results of SG Tube ISI Conducted in Apr 1998.Rept Includes Description of Number & Extent of Tubes Inspected,Location & Percent wall-thickness Penetration for Each Indication of Imperfection ML20205L2031999-03-26026 March 1999 Submits Correction to Dose History of Tj Chambers.Dose Records During 1980-1997 Were Incorrectly Recorded Using Wrong Social Security Number.Nrc Form 5 Not Encl ML20205C7371999-03-25025 March 1999 Certifies That Dbnps,Unit 1,plant-referenced Simulator Continues to Meet Requirements of 10CFR55.45(b) for Simulator Facility Consisting Solely of plant-referenced Simulator.Acceptance Test Program & Test Schedule,Encl ML20205E3551999-03-19019 March 1999 Requests That Proposed Changes to TS 6.8.4.d.2 & TS 6.8.4.d.7 Be Withdrawn from LAR Previously Submitted to NRC ML20204J6361999-03-17017 March 1999 Forwards Firstenergy Corp Annual Rept for 1998 & 1999 Internal Cash Flow Projection as Evidence of Util Guarantee of Retrospective Premiums Which May Be Served Against Facilities PY-CEI-NRR-2375, Forwards List That Details Util Insurers,Policy Numbers & Coverage Limits for Two Power Plants,Per Requirements of 10CFR50.54(w)(3) Re Reporting of Property Insurance Coverage1999-03-15015 March 1999 Forwards List That Details Util Insurers,Policy Numbers & Coverage Limits for Two Power Plants,Per Requirements of 10CFR50.54(w)(3) Re Reporting of Property Insurance Coverage ML20204E6821999-03-12012 March 1999 Requests That Listed Changes Be Made to NRC Document Svc List for Davis-Besse Nuclear Power Station,Unit 1 1999-09-09
[Table view] Category:UTILITY TO NRC
MONTHYEARML20065D0491990-09-14014 September 1990 Forwards Operator & Senior Operator Licensing Exam Ref Matl for Exam Scheduled for Wk of 901112,per 900607 Request ML20065D4951990-09-14014 September 1990 Forwards Updated Exam Schedule for Facility,In Response to Generic Ltr 90-07, Operator Licensing Natl Exam Schedule ML20059K4681990-09-14014 September 1990 Provides Supplemental Info Re Emergency Response Data Sys (Erds).Data Transmitted by Util ERDS Will Have Quality Tag of 4 & Point Identification for ERDS Renamed ML20059G2341990-09-10010 September 1990 Provides Response to Request for Addl Info Re Interpretation of Tech Spec 3/4.7.10, Fire Barriers. Interpretation Is Implemented & Unnecessary Compensatory Measures Removed.List of Fire Barriers Inspected on One Side Only Encl ML20059G4961990-09-0606 September 1990 Submits Voluntary Rept of Svc Water HX Testing During Sixth Refueling Outage.Expected Flow Rates Not Achieved.Periodic Tests Developed to Check Efficiency of Containment Air Coolers ML20064A6271990-09-0606 September 1990 Requests That Requirement Date for Installation & Testing of Alternate Ac Power Source & Compliance w/10CFR50.63 Be Deferred Until Completion of Eighth Refueling Outage ML20028G8611990-08-28028 August 1990 Forwards Davis Besse Nuclear Power Station Semiannual Rept: Effluent & Waste Disposal,Jan-June 1990. ML20059D4121990-08-28028 August 1990 Forwards Second 10-Yr Interval Pump & Valve Inservice Testing Program ML20059D5521990-08-24024 August 1990 Forwards Semiannual Fitness for Duty Rept for Jan-June 1990 ML20059B5291990-08-23023 August 1990 Forwards Updated Fracture Mechanics Analysis of Hpi/Makeup Nozzle,Per 900510 Meeting W/Nrc.Util Believes That Addl Analysis to Assess Structural Integrity of Nozzle Using More Conservative Fracture Model Supports Previous Analysis ML20058Q3911990-08-16016 August 1990 Requests NRC Concurrence on Encl Interpretation & Technical Justification of Tech Spec 3/4.7.10, Fire Barriers ML20058P7801990-08-10010 August 1990 Advises of Intentions to Revise Testing Requirements for Fire Protection Portable Detection Sys at Plant & Functional Testing of auto-dialer & Telephone Line Subsys from Daily to Weekly Testing ML20063P9981990-08-0909 August 1990 Submits Supplemental Response to Insp Rept 50-346/89-21. Util Rescinds Denial & Accepts Alleged Violation ML20056A5341990-08-0303 August 1990 Confirms Electronic Transfer of Payment of Invoice I0942 Covering Annual Fee for FY90,per 10CFR171 ML20058M7791990-08-0303 August 1990 Forwards Rev 10 to Industrial Security Plan & Rev 6 to Security Training & Qualification Plan.Revs Withheld ML20058L1821990-08-0101 August 1990 Forwards Davis-Besse Dcrdr Human Engineering Discrepancy Repts 1988 Summary Addendum 1,Vol 1, Per NRC Audit Team Request ML20056A8341990-07-23023 July 1990 Forwards Revised Monthly Operating Rept for June 1990 for Davis-Besse Nuclear Power Station Unit 1 ML20055H4601990-07-20020 July 1990 Discusses Resolution of Draft SER Open Item on Voluntary Loss of Offsite Power.Util Preparing License Amend Request Per Generic Ltrs 86-10 & 88-12 to Relocate Fire Protection Tech Specs & Update Fire Protection License Condition ML20055F9681990-07-17017 July 1990 Forwards Application for Amend to License NPF-3,adding Centerior Svc Company as Licensee in Facility Ol.Change Allows for Improved Mgt Oversight,Control & Uniformity of Nuclear Operations ML20055F8561990-07-17017 July 1990 Discusses Util Planned Activities Re Instrumented Insp Technique Testing Performed at Facility in View of to Hafa Intl.Relief Requests Being Prepared by Util for Sys on Conventional Hydrostatic Testing ML20044B3001990-07-12012 July 1990 Provides Written Confirmation of Util Electronic Transfer of Funds to NRC on 900711 in Payment of Invoice Number I1050 ML20044B1841990-07-10010 July 1990 Requests Approval of Temporary non-code Repair & Augmented Insp of Svc Water Piping,Per 900626 Telcon ML20055D9701990-06-29029 June 1990 Provides Written Confirmation of Util Electronic Transfer of Funds for Payment of Invoice 0111 Covering Insp Fees for 890326-0617 ML20043H5291990-06-14014 June 1990 Forwards Plans Re Reorganization & Combining of Engineering Assurance & Svc Program Sections ML20055C7521990-06-14014 June 1990 Responds to NRC Bulletin 89-002, Potential Stress Corrosion Cracking of Internal Preloaded Bolting in Swing Check Valves & Justification for Alternate Insp Schedule for One Valve. No Anchor Darling Swing Check Valves Installed at Plant ML20055F2261990-06-14014 June 1990 Forwards 1990 Evaluated Emergency Exercise Objectives for Exercise Scheduled for 900919 ML20043G5661990-06-14014 June 1990 Forwards Rev 9 to Industrial Security Plan.Rev Withheld (Ref 10CFR73.21) ML20043G7811990-06-12012 June 1990 Forwards Info Re Implementation of NUREG-0737,Item II.F.2, Inadequate Core Cooling Instrumentation, Per NRC 900214 Safety Evaluation.Item II.B.1 Issue Re Reactor Vessel Head Vent Also Considered to Be Closed ML20043F6091990-06-11011 June 1990 Forwards Util Comments on NRC Insp Rept 50-346/90-12, Per 900601 Enforcement Conference Re Core Support Assembly Movement & Refueling Canal Draindown.Refueling Canal Draindown Procedure Provides Specific Draining Instructions ML20043E1301990-06-0101 June 1990 Withdraws 870831 & 890613 Applications to Amend License NPF-3.Changes Requested Addressed by Issuance of Amend 147 or Can Now Be Made as Change to Updated SAR Under 10CFR50.59 ML20043D5601990-05-31031 May 1990 Forwards Application for Amend to License NPF-3,revising Tech Spec 3/4.6.4.1, Combustible Gas Control - Hydrogen Analyzers. Request Consistent W/Nrc Guidance,Generic Ltr 83-37,dtd 831101,NUREG-0737 Tech Specs & Item II.F.1.6 ML20043D5691990-05-31031 May 1990 Forwards Application for Amend to License NPF-3,requesting Extension of Expiration Date of Section 2.H to Allow Plant Operation to Continue Approx 6 Yrs Beyond Current Expiration Date ML20043D1451990-05-31031 May 1990 Forwards Rev 11 to Updated SAR for Unit 1.Rev Updates Table 6.2-23 Re Containment Vessel Isolation Valve Arrangements ML20043D1621990-05-29029 May 1990 Documents Util Understanding of NRC Interpretation of Plant Tech Spec 3.7.9.1,Action b.2 Re Fire Suppression Water Sys, Per 891206 Telcon.Nrc Considered Electric Fire Pump Operable Provided Operator Stationed to Open Closed Discharge Valve ML20043C2331990-05-25025 May 1990 Forwards Summary of 900510 Meeting W/B&W & NRC in Rockville, MD Re Hpi/Makeup Nozzle & Thermal Sleeve Program.List of Attendees & Meeting Handout Encl ML20043B1701990-05-18018 May 1990 Forwards Revised Exemption Request from 10CFR50,Section III.G.2,App R for Fire Areas a & B,Adding Description of Specific Limited Combustibles That Exist Between Redundant Safe Shutdown Components in Fire Area a ML20043A5441990-05-16016 May 1990 Discusses Status of Safety & Performance Improvement Program Portion of B&W Owners Group EOP Review Project ML20043A2311990-05-11011 May 1990 Responds to Violation Noted in Insp Rept 50-346/90-08. Corrective Actions:Results of Analysis of Radiological Environ Samples & Radiation Measurements Included in 1989 Annual Radiological Environ Operating Rept ML20043A4901990-05-10010 May 1990 Forwards Summary of Differences Between Rev 5 to Compliance Assessment Rept & Rev 1 to Fire Area Optimization,Fire Hazards Safe Shutdown Evaluation, Vols 1-3.Rept Demonstrates Compliance W/Kaowool Wrap Removal ML20042F9801990-05-0404 May 1990 Provides Written Confirmation of Util Electronic Transfer of Payment of Invoice Number 10716 to Cover Third Quarterly Installment of Annual Fee for FY90 ML20042F5781990-05-0303 May 1990 Provides Status of Hpi/Makeup Nozzle & Thermal Sleeve Program.Nrc Approval Requested for Operation of Cycle 7 & Beyond Based on Program Results.Visual Insp of Thermal Sleeve Identified No Thermal Fatique Indications ML20042F0951990-04-30030 April 1990 Responds to Violations Noted in Insp Rept 50-346/90-02. Corrective Actions:Maint Technician Involved in Tagging Violation Counseled on Importance of Procedure Adherence W/ Regard to Personnel Safety ML20042F0841990-04-27027 April 1990 Responds to Violations Noted in Insp Rept 50-346/89-201 for Interfacing Sys LOCA Audit on 891030-1130.Corrective Actions:Plant Startup Procedure Will Be Revised Prior to Restart from Sixth Refueling Outage ML20042E7311990-04-27027 April 1990 Forwards Application for Amend to License NPF-3,deleting 800305 Order Requiring Implementation of Specific Training Requirements Which Have Since Been Superseded by INPO Accredited Training Program ML20042F1961990-04-27027 April 1990 Informs of Adoption of Reorganization Plan Re Plants on 900424.Reorganization Will Make No Changes in Technical or Financial Qualifications for Plants.Application for Amends to Licenses Adding Company as Licensee Will Be Submitted ML20043F7261990-04-20020 April 1990 Requests Exemption from 10CFR55.59(a)(2) to Permit one-time Extension of 6 Months for Reactor Operators & Senior Reactor Operators to Take NRC 1990 Requalification Exam. Operators Will Continue to Attend Training Courses ML20042E7091990-04-17017 April 1990 Forwards Annual Environ Operating Rept 1989 & Table 1 Providing Listing of Specific Requirements,Per Tech Spec 6.9.1.10 ML20012F5091990-04-0303 April 1990 Forwards Completed NRC Regulatory Impact Survey Questionnaire Sheets,Per Generic Ltr 90-01 ML20012F6001990-04-0202 April 1990 Submits Supplemental Response to Station Blackout Issues,Per NUMARC 900104 Request.Util Revises Schedule for Compliance W/Station Blackout Rule (10CFR50.63) to within 2 Yrs of SER Issuance Date ML20012E0181990-03-22022 March 1990 Forwards Application for Amend to License NPF-3,changing License Condition 2.C(4) Re Fire Protection Mods to Fire Extinguishers,Fire Doors,Fire Barriers,Fire Proofing,Fire Detection/Suppression & Emergency Lighting 1990-09-06
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l TC'.EDO i EDISON Rowto P. Cmw License No. NPF-3 v. . n .,,,,
una Docket No. 50-346 "8'""
Serial No. 899 February 2, 1983 Mr. John F. Stolz, Chief Operating Reactors Branch No. 4 Division of Licensing U. S. Nuclear Regulatory Commission Washington, D. C. 20555
Dear Mr. Stolz:
This is in response to your Ictter dated December 27, 1982 (log No. 1165) relating to plant computer system and NNI-X power failure. Your letter requested information on operability of plant ccmputer system in the event of unavailability of YAU or YBU and the implications of a loss of NNI-X power supply transient. Attachment 1 provides Toledo Edison's response to -
your letter as relating to th; Davis-Besse Nuclear Power Station Unit 1.
Very truly yours.
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RPC:SCJ:llA cc:
DB-1 NRC Resident Inspector 8302070369 930202 PDR ADOCK 05000346 P PDR THE TOLEDO EDIGON COMPANY EDISDN PLAZA 300 MADISON AVENUE TOLEDO, OHIO 43G52 l
l
Licance No. NpF-3 Docket No. 50-346 Serial No. 899 February 2,.1983 '
Attachment I to Toledo Edison Letter to the NRC on plant Computer System and Loss of NNI-X Item 1: Toledo Edison Company letter dated July 8, 1981 committed to providing automatic transfer to a redundant power source for the control room annunciator system. We understand that this commitment is fully implemented. Toledo Edison Company also committed to a similar provision for the plant computer system which was to be implemented when the new plant computer was installed. We understand that the new computer was installed during the last refueling outage.
Toledo Edison Company is requested to describe how the commitment for the plant computer system has been impic-mented. Specifically, does the computer system remain functionally operable (cpu, I/O units, etc.) from the control room in the event either power supply (YAU or YBU) is unavailable? If the commitment la not yet fully imple-mented, describe the extent to which the present system operability is independent of a single power source, the nature of your intended actions to complete impicmentation, your schedule for completion; and thc compensatory measures in force in the interim.
Response: The overall replacement of the plant computer system has several phases, phase one was completed during 1982, when the central processor and all peripherals except the multiplexers were replaced.
In 1982 Toledo Edison installed two separate processors, each powered from an independent uninterruptible power supply (YAU or YBU) source. power for the operator displays and peripherals has been divided equally between YAU and YBU. Both processors are normally running in a master / slave mode with a direct communication link between them.
During loss of YAU or YBU, af ter a 5 second period, the powered processor becomes the master and transfers all operator peripherals to its I/O buss. The computer multi-plexers have not been upgraded to meet the singic power failure criteria. Toledo Edison intends to provide this protection when the multiplexers are replaced.
The additional modifications providing the single failure protection for the plant computer system will be implemented in accordance with an integrated schedule approach that will maximize resources. The compensatory measure in force in the interim consists of reliance on manual comput-ation in the event of loss of a single power source.
+
Licensa-No. NPF-3 Docket No. 50-346 Serial No. 899 February 2, 1983 I
No direct or indirect reactor protection or process control i
action is taken by the computer system. The primary function of the system is to provide information to assist the operator in efficient operation of the plant. Should the computer be completely out of service for any reason, the capability of plant operation or safe shutdown under automatic or manual control is not impaired.
Item 2: It is our understanding that a large fraction of the non-nuclear instrumentation is powered from the NN1-X supply and the remainder from tne NNI-Y supply. Therefore, if the NNI-Y supply fails, a minor plant transient would occur and that a plant trip might be avoidable. Accordingly, control room reedout devices are switched to NNI-X powered transmitters to provide sufficient information to the reactor operator. However, if NNI-X supply fails, the plant transient is more significant and a plant trip is
-unavoidable.
Toledo Edison Cempany is requested to describe the transient that occurs (in terms of RCS pressure, temperatures and flows, etc.) if NNI-X is lost. Identify the control room indicators rematting to permit identification of the l transient, track the course of the event. Identify those l plant systems necessary to mitigate the transient. Identify any systems that are expected to be unavailble during the event. Provide your basis for acceptability of this event in lieu of plant modifications or other compensatory actions to lessen the effects of the disproportionate NNI loading on the NNI-X power supply.
Response: The NNI cabinets are provided with automatic transfer switches that select a redundant source of AC power if the normal source is lost. This feature, plus redundant DC power supplies, makes a loss of power unlikely.
A loss of NNI-X AC/DC power supply causes main feed water flows in both loops to be BTU limited to apprcximately zero feed water flow. The reactor coclant system average c temperature (Tave) input to the Integrated Control System i (ICS) falls mid-ncale to 570*F resulting in continuous withdrawal of control rods. The above actions culminate in a hip,h pressure condition in the reactor coolant system causing a reactor trip. The main and startup feed water flow control will be lost and the secondary side inventory will begin to rapidly boil off. Manual or automatic initiation of the Steam and Feedwater Rupture Control System (SFRCS) will restore secondary side cooling, and safety grade secondary side level control.
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1.icenze No. NPF-3 Docket No. 50-346 Serial No. 899 -
February 2, 1983 Davi's-Besse Unit i experienced a loss of NNi-X AC power on January 18, 1983. This trannient van very similar to the onn dencribed abovo. Further detailed evaluation of this trannient in continuing.
The loss of NNI-X AC/DC results in the failure of a algnifi-cant number of controlling signals which results in a ynir trip and possible SFRCS actuation. The following are the pertinent controlling nignal ..nd the resul. ting effects na a result of loss of NNI-X AC and NNI-X DC:
A. loss of NNI-X AC
- 1. Tave Integrated Control System input falls to 570*F causing control rods to continuounty withdraw nince normal Tave is maintained at 582*F.
- 2. Selected turbine header pressure signal fails to 900 psig causing turbine load increano as normal turbine header ,ressura is maintained at 870 poig.
- 3. l.oop and selected Tg nignals f all to 570*F causing both loop main feed water flown to be BTtl limited to approximately zero feed water flow (lons of main feed water flow to both steam generators). To compensate for thin, the loop and selected Tg nignaln are proce-durally transferred to NNI-Y.
- 4. Reactor trip on high pressure.
- 5. Pont trip tenponse is off-normal due to failure of steam generator low level limits and fallere of makeup flow control valve MU32 "an is" (approximately 25%
open normally).
- 6. Possible SFRCS actuation on low steam generator level due to failure of steam generator low level limit control by the Integrated Control System. (Start up range level signal to the ICS is f ailed at cent::r ncale and will not actuate steam generator low level limit control unless action in taken by the operator).
The SFRCS actuation will ret. tore adequate secondary side cooling and level control.
- 7. Ponnible initiation of Safety Featuren Actuation System (SFAS).
i
License No. NPF-3 Docket No. 50-346 Serial No. 899 -
February 2, 1983 The following automatic functions will become inoperable j following loss of NNI-X AC:
- 1. Automatic pressurizer level control is inoperable duc to makeup flow control valve MU32 failing "as is" and inaccurate pressurizer level control signal to MU3?.
To alleviate this situation, operator is procedurally L directed to use the MU32 bypass valve (MU211) utilizing the control room pressurizer level indication. The !
control room pressurizer level indicators will indicate the existing uncompensated pressurizer level.
- 2. Automatic seal injection flow control is inoperable due to seal injection valve (MU19) failing "as is". !
- 3. The seal injection flow interlock will not function to prevent the start of a reactor coolant pump without >
seal injection flow, houever, the reactor coolant ;
pumps will not trip resulting from this loss of .
function. i
^ i
- 4. Pressurizer low level heater cutoff will not function.
However, manual control of the safety grade heaters f rom the control room will not be impaired. l S. Steam Generator low level limit control will not t l function due to steam generator startup range level j signals to the Integrated Control System failing to 125 inches. However, the control room and auxiliary ;
shutdown panel steam generator start up range level I indicators will be available and will display the existing steam generator water levels. t
- 6. All automatic feed water flow control (both main and startup) will be inoperable due to failed signals ,
and/or faulty temperature compensation. However, ,
essential auxiliary feed water controls in the control
) room and controls at the auxiliary shutdown parel will be available.
B. Loss of NNI-X DC j
- 1. Tave Integrated Control System input fails to 570*F causing control rods to continuously withdraw since ;
normal Tave is maintained at 582*F. ;
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Licenze No. NPF-3 Docket No. 50-346 Serial No. 899 February 2, 1983
- 2. Selected turbine header pressure signal fails to 900 psig causing the turbine to continuously pick up load.
- 3. Loop and selected T signals fail to 570*F causing H
both loop main feed water flows to be BTU limited to approximately zero feed water flow (loss of main feed water flow to both steam generators).
- 4. If open, the pressurizer spray valve (RC2) and the PORV (RC2A) will close. The POEV can, however, be manually opened if required.
- 5. If energized, pressurizer heaters will turn off.
Manual control of the safety grade heaters from the control room will not be impaired.
- 6. Reactor trip on high pressure.
/. Makeup flow control valve MU32 will fail to 50% open.
- 8. Possible SFRCS r.ctuation on low steam generator IcVel due to failure of steam generator low level limit contrel by the Integrated Control System (start up range level signal to the Integrated Control System is failed at center scale will not actuate low level limit control, and cannot be regained without NN1-X DC power). This will restore adequate secondary side cooling and level control.
- 9. Possible initiation of Safety Features Actuation System.
The following automatic functions will become inoperable following loss of NNI-X DC:
- 1. Automatic pressurizer level control is inoperable due to makeup flow control valve MU32 failing to 50% open and inaccurate pressurizer level control signal to MU32. To alleviate this situation, operator is procedurally directed to use the MU32 bypass valve (MU211) utilizing the control room pressurizer level indication. The control room pressurizer level indicators will indicate the existing uncompensated pressurizer level.
- 2. Automatic seal injection flow control is incperable due to seal injection valve MU19 failing to 50% open (approximately the normal position for this valve).
Licanes No. NPF-3 Docket No. 50-346 Serial No. 899 February 2, 1983
- 3. The seal injection flow interlock will not function to prevent the start of a reactor coolant pump with out seal injection flow, however, the reactor coolant pumps will not trip resulting from this loss of function.
- 4. Pressurizer low level heater cutoff will not function.
However, no damage will be impar:cd to the heaters since they will be de-energized. In addition, manual control of the safety grade heaters from the control room will not be impaired.
- 5. Pressurizer heaters will not function in the automatic mode, however, manual control of the safety grade heater banks can be regained in the control room.
- 6. Neither the pressurizer spray valve (RC2) nor the PORV (RC2A) will open automatically. The PORV can, however, be manually opened if required.
- 7. Steam generator low level limit control will not function due to steam generator etartup range level signals to the Integrated Control System failing to 125 inches. The safety grade control room and auxiliary shutdown panel startup level indicators will display existing steam generator levels.
- 8. All automatic feed water flow control (both main and scartup) is inoperable due to failed signals and/or faulty temperature compensation. However, essential auxiliary feed water controls in the control room and controls at the auxiliary shutdown panel will be available.
- 9. Decay Heat / Low Pressure Injection pump 1-2 high and low flow alarts are inoperable.
- 10. High Pressure Injection pump 1-2 high and low flow alarms are inoperable.
- 11. Loop 2 high and low reactor. coolant pressure alarms '
are inopere'ile.
To avoid a severe plant transient caused by a loss of NNI-X, there are sufficient alarms to alert the operator about such failure which may permit operator action that could avoid a potential SFRCS actuation. This will result I in a reduced cooldown rate of the reactor coolant system which will slow the transient to a more controllable rate under the limiting circumstances. The alarms are:
P License No. NPF-3 Docket No. 50-346 Serial No. 899 February 2, 1983 A. NN1-X AC:
- 1. ICS/NNI 118 V AC PWR Trill. Annunicator Alarm
- 2. I.ons of X-AC NNI Power Indicating 1.ight on Control Room Panel
- 3. Computer point Q696-NNI X 118 V AC PWR Trill.
- 4. ICS S/C 1 and ICS S/C 2 on 11TU l.imit Annunicator alarma
- 5. Zero volta indicated on Uninterruptible Instrument hunnen YAU and YllU
- 6. On al1 X-NNI powered recordern, the penn fail "an in" and paper motion stopa
- 7. All X-powered ludicatorn falla toward, but not necennarily at, center scale.
11 . NNI-X DC:
- 1. l.oss of X-DC NNI Power Indicating 1.ight on Control Hoom Panel
- 2. NNI 24 VDC llun Trip Annunicator alarm
- 3. Computer Point Q715 - NNI-X DC llun Trip
- 4. RC I.oop 2 Ilot 1.cg l'!nw 1.ow Annunciator alarm
- 5. RC llot 1.cg Total Flow !.ow Annunicator alarm
- 6. ICS S/G 1 and ICS S/C 2 on llTU l.imit Annunciator alarm
- 7. ICS RC Flow Runback in Effect Annuneintor alarm
- 8. All indicators and recordern displaying X signals f ail toward, but not necennarily at, center scale, llaned on the above, we feel that there are sufficient alarms and luuications available to the operator to take appropriate immediate as well as supple-mentary actions as required to mitigate the trannient, in order to enhance the overall reliability of the NN1-X AC and DC power supplien, Toledo Edinon han undertaken several measuren. These include:
! 1. Providing automatic trannfer of the AC nource to an alternate unin-terruptible power source when the primary source has been lost.
- 2. Providing two NNI-X DC power supplien which are nupplied f rom separate uninterruptible AC sources. Each DC power supply can supply the full load of the system.
- 3. Another modification, in the design stage, in to provide independent funen (see attached figure) to the AC circults auch that failure in one portion of NNI-X will not cause a total NNI-X failure, and no l more than one critical component will be lont
License No. NPF-3 Docket No. 50-346 Serial No. 899 February 2, 1983 The system modifications completed heretofore, and those under evaluation provide sufficient compensatory measures to enable appropriate operator actions to ensure acceptable system respcnse in relation to the severity of overall transient, be d/9 l
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