ML18039A233
ML18039A233 | |
Person / Time | |
---|---|
Site: | Browns Ferry |
Issue date: | 01/02/1998 |
From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
To: | |
Shared Package | |
ML18039A230 | List: |
References | |
50-259-97-11, 50-260-97-11, 50-296-97-11, NUDOCS 9801210278 | |
Download: ML18039A233 (64) | |
See also: IR 05000259/1997011
Text
U.S.
NUCLEAR REGULATORY COMMISSION
REGION II
Docket Nos:
License
Nos:
Report
Nos:
Licensee:
Facility:
Location:
Dates:
Inspectors:
50-259,
50-260,
50-296
50-259/97-11,
50-260/97-11,
50-296/97-11
Valley Authority
Browns Ferry Nuclear Plant,
Units 1, 2,
8 3
Corner of Shaw and Browns Ferry Roads
Athens,
35611
October
26 - December
6,
1997
L. Wert, Senior Resident 'Inspector
J. Starefos,
Resident
Inspector
E.
Di Paolo.
Resident
Inspector
E. Girard,
Reactor
Inspector
(Section
E1.3)
Accompanying Personnel:
T. Scarbrough,
R.
Wessman,
Approved by:
M. Lesser,
Chief
Reactor Projects
Branch
6
Division of Reactor
Projects
980i2i0278 980i02
ADQCK 05000259
8
0
EXECUTIVE SUMMARY
Browns Ferry Nuclear Plant, Units 1, 2,
8 3
NRC Inspecti'on Report 50-259/97-11,
50-260/97-11.
50-296/97-11
This integrated
inspection included aspects
of licensee
operati'ons,
engineering,
maintenance,
and plant support.
The report covers
a six-week
period of resident inspection
and
an inspection of the licensee's
motor-
operated
valve
(GL 89-10) program.
~0er ati ons
Operator actions in response
to a Unit 2 single control rod insertion
and
reactor
scram were good.
Procedures
were actively referenced
and correctly
followed.
Good performance
was noted
on the part of the assistant
unit
operator that identified an
EHC fluid leak during performance of rounds.
,(Section 01.1)
Procedural
controls of the control
room emergency ventilation
(CREV) system
priority selector
swi,tch were not adequate
to ensure that the switch was
maintained in the correct position.
(Violation 260,296/97-11-02,
Failure to
Control
CREV Switch Position,
Section 01.3)
Further review is necessary
regarding testing, of the transfer control circuitry.
(Unresolved
Item
260,296/97-11-03,
Adequacy of CREV Standby Train Circuit Testing,
Section
01.3)
Two examples of status
control issues
were identified by the inspectors
during
this inspection.
The first example is addressed
by the violation for
inadequate
control of the
CREV system priority selector switch.
In addition,
the inspectors identified
a drain valve on
a non-safety related service air
compressor that was not .in the requi red position.
Additional
NRC review of
recent status control issues is warranted.
( Inspection Followup Item
260,296/97-11-01,
Status
Control Issues,
Section 01.2).
Adequate
mechanisms
were in place to prompt an annual
licensee
review of
freeze protection equipment.
Small bore and stagnant
piping in
RHRSW pump
rooms could have been given priority during inspection
and repai r of freeze
protection equipment
so that the identified condition of uninsulated
small
bore piping in colder conditions would not have existed.
The licensee'.s
actions to place heaters
in and tarpaul.ins
over the
RHRSW pump rooms provided
a level of protection for the uninsulated piping.
(Section 02.3)
Maintenance
Good mechanical
maintenance
performance
was noted during replacement of the
immersion heater coil assembly
on the 28
EDG.
Effective troubleshooting to
determine the cause of burned lugs in the
EOG control cabinet identified
problems with the immersion heater
even though the heater
appeared to be
working.
(Secti on Ml.1)
ill
il~
~E
Implementation of Generic Letter 89-10 at Browns Ferry was not sufficiently
complete to permit the
NRC to complete its review.
(Section E1.3)
Inspectors identified that the licensee failed to revise procedures
to declare
the applicable
system or train inoperable
when certain motor-operated
valves
'ere
p')aced in their non-safety positions
(Section E1.3)
Inspectors identified that the licensee failed to prepare motor-operated
valve
trend reports in accordance
with procedure
requirements.
(Section E1.3)
The licensee failed to evaluate test data to assess
its:Generic Letter 89-10
program design
assumptions
and improperly used actuator stall efficiency in
evaluating motor-operated
valve operability.
(Section E1.3)
On two occasions
during the inspection period, the
NRC prompted problem
evaluation reports
(PERs) to be written.
The first example
was
an
NRC
identified deficiency with a main steam pressure
instrument calibration
calculation.
The original set point and scaling calculation for the main
steam pressure
instruments
analyzed for a calibration frequency of 12 months
versus the surveillance instruction frequency of 18 months.
(Section
E1. 1)
The second
example involved problems with radiation monitor RH-90-130.
(Section
R2. 1)
In both of these
examples,
personnel
did not initiate PERs
when they were warranted.
Review of the technical operability evaluation
(TOE) to evaluate the main
steam line pressure
transmitters,
which were installed in the plant with
incorrect upper range pressure limits, identified deficiencies with the TOE.
The overall results of the
TOE were not affected.
No regulatory violations
were identified concerning these non-safety related transmitters.
(Section
El. 1)
The licensee properly implemented the Core Operating Limits Report for Unit 2
Cycle
10 with respect to the revised
TS requirements.
(Section
E1.2)
The licensee's
incident investigation
team performed well in investigating the
equipment
issues
which caused
the Unit 2 scram.
The team studied available
information, developed
a theory of the cause,
and in a prompt manner,
performed electrical testing which supported the postulated
cause.
The
investigation into the
EHC fluid leaks
was also thorough
and determined the
cause of the leaks in a reasonable
time period.
(Section
E2. 1)
Although the licensee's
actions to decrease
the oil particulate levels in the
RCIC system were adequate.
the
RCIC oil particulate
level issue represents
another
example of the difficulties that the licensee is experiencing with the
lube oil analysis
program.
(Section E2.2)
ili
Pl ant
Su
ort
Unexpected indications
on the radioactive effluent monitor recorder were not
thoroughly investigated prior to discontinuation of compensatory
actions
required for an inoperable monitor.
The licensee
subsequently
completed
a
detailed
investigation which identified that
a leaking valve had caused the
unexpected
indications.
The investigation 'also concluded that the monitor
was not inoperable
and that regulatory requirements
were met during the
period.
(Section R2.1)
ili
0
Summar
of Plant Status
Re ort Details
Unit 1 remained in a long-term lay-up condition with the reactor defueled.
Unit 2 was brought critical on October
18,
1997. following the cycle 9
refueling outage.
The unit reached full power on October
23.
1997.
Electro-
hydraulic control fluid leaks
on turbine control valves
caused
several
power
decreases
to perform maintenance
during the inspection period.
(Section
E2. 1)
On October 28,
1997. the unit scrammed
when
a
(RPS) relay problem occurred while a half scram
was already present
on the A
RPS system.
(Sections
01. 1,
E2. 1)
The unit was brought critical on October
30,
1997,
and remained at power during the inspection period with the
exception of maintenance
and routine testing
Unit 3 operated
at power with the exception of routine testing
and several
balance of plant maintenance
issues
which required
power decreases.
I. 0 erations
01
Conduct of Operations
01. 1
Unit 2 Sin le Control
Rod Insertion
and Reactor
a.
Ins ection Sco
e
71707 93702
The resident. inspectors
observed
and reviewed the actions of control
room operators
in response
to two separate
unexpected
plant transients.
In one instance,
a single control rod inserted
unexpectedly
during
repairs of an electrohydraulic
(EHC) fluid leak.
Not directly related
to this incident.
an automatic reactor scram occurred shortly thereafter
due to a problem wi.th reactor protection system relays.
Additional
inspection regarding the cause of the scram is described
in section
E2. 1
of this report.
b.
Observations
and Findin s
At 12:23 p.m.,
on October 28,
1997,
an Assistant Unit Operator, noted
a
decreased
Unit 2
EHC fluid .reservoir level.
It was determined that an
EHC oil leak existed
on the servo mechani.sm for the gl turbine control
valve.
Reactor
power was reduced to allow the valve to be shut for
repai rs.
Upon closing the Pl control valve,
an expected half scram was
received
on
RPS channel
A.
Approximately 2 minutes after receiving the
half scram, control rod 30-23 moved in to the full overtravel position.
One of the resident inspectors
was in the control
room at the time and
observed the rod: insertion.
The inspector
noted that the rod appeared
to travel
from the full out position to the full overtravel position in
less than
5 seconds.
The licensee
commenced corrective actions for the
ili
01.2
2
1
rod drift in accordance with Abnormal Operating Instructi.on,
2-AOI-85-2,
Uncoupled Control
Rod.
This included evaluating thermal limits and
inspecting the
CRD hydraulic control unit (HCU) for abnormalities.
Subsequent
inspection, revealed that the
control rod 30-23 was leaking air past its diaphragm.
The licensee
postulated that air pressure
on the scram val.ve was
r educed
by leakage
through this path
and leakage
through 'the "B" powered
scram solenoid
ilot valve (SSPV).
The "A" powered
SSPV was de-energized
due to the
alf scram.
This caused
the scram valve to open
and resulted in the rod
insertion.
At 2:50 p.m., repairs
were completed
on the gl Control Valve (CV).
The
valve was opened
and the half scram
on
RPS channel
A was reset.
At 3:08
PH the operators
reshut the gl CV in order to perform post maintenance
testing.
About
1 minute later, concurrent with the worker releasing
a
button to re-open the
gl CV, the reactor
scrammed.
Operators
completed
scram follow up actions satisfactorily.
Reactor water level decreased
to lowest level of about
-32 inches
and was rapidly restored
by the
pumps.
The response of the feedwater
pumps
was
as expected
following the scram.
No safety system problems were observed
associated
with the recovery.
Additional review of,the scram. is described
in
Section
E2.1.
Following the Unit 2 scram,
both SSPVs
and the scram outlet valve
responsible for the single rod insertion,
were replaced.
One
,of the inspectors
observed satisfactory
scram time testing of the 30-23
control
rod after the work was completed.
Following completion of
corrective actions
(see section
E2. 1),
a reactor
startup
was
commenced
late on October 29,
1997.
Operator performance
and control
room
conduct were observed to be good during the rod withdrawal to
criticality.
Conclusions
The actions oi the control
room operators
in response to these
unexpected
were good.
Procedures
were actively referenced
and correctly followed. The
EHC fluid leak was identified by an
during the performance of rounds.
Status
Control of 0 erations
E ui ment
Ins ection Sco
e
71707
The inspectors
reviewed the licensee's
corrective actions after
an
incorrectly positioned service air system valve was identified by the
NRC.
Observations
and Findin s
On November 10,
1997.. the inspectors identified that
a drain valve on
the
F service air compressor after-cooler condensate
trap was partially
open
and discharging
a water/air mixture.
This valve had previously
ili
been caution tagged in the throttled open position to remove moisture
buildup since the licensee believed that the trap was not operating
properly.
The caution tag was subsequently
removed
and the valve was
expected to be shut.
The trap is
a float type trap.
The drain valve
drains water from the trap body (vice other designs
which drain from
upstream of the trap).
Operation of the trap bypass will drain water
from the trap body, thus it will take
some time for the body to fill
back up and
commence
automatic trap operation again.
The licensee initiated
a Problem Evaluation Report
(PER) to investigate
the cause of the mispositioned valve.
Operations
management
postulated
that an Assistant Unit Operator
opened the valve to check for moisture
and upon finding a significant quantity of liquid, left it throttled to
complete draining with the intention of returning later to close it.
Although the valve was not in the correct position and did affect the
operation of the trap, overall operation of the service air system
was
not adversely affected.
The
PER evaluation
noted several
other
mispositioned
component incidents since January
1996.
The
PER
corrective actions include
a discussion of the
PER and event with all
shift crews, stressing
the need for open
and honest
communication
concerning errors
and events.
The Operations
Superintendent will
evaluate the use of red valve covers
on valves in the vicinity to act as
a reminder to the operator to re-close the valve.
Operation of this
particular trap with be covered during
AUO requalification training.
Also, the
PER corrective actions indicated that
an engineering
work
request
was issued to address
the adequacy of the condensate
traps
and
the excessive
moisture experienced with the new compressors.
Conclusion
The equipment identified out of the required position was not safety-
related.
The involved equipment
remained operable.
However,
NRC
inspectors identified two examples of status control issues
during the
inspection period.
(See Section 01.3 for the second
example.)
In
recent months, the licensee
has identified other status control issues.
Further review of recent status control issues is warranted.
(Inspection Follow up Item (IFI) 50-260,296/97-11-01,
Status
Control
Issues.)
Control
Room Emer enc
Ventilation S stem Preferred Train Selector
Switch Issues
Ins ection Sco
e
71707
37551
The inspectors
reviewed the effect of having the Control
Room Emergency
Ventilation (CREV) pref'erred selector switch in a position other
than
that required
by work instructions.
Surveillance testing
was reviewed
to determine if the automatic start feature of the
CREV unit was
adequately tested.
ili
0
b.
Obser vati ons
and Findin s
On November
19,
1997,
one of the resident
inspectors identified that the
.CREV system priority selector
switch (0-XSW-031-7214)
was in a position
different than that described in work control instructions.
Work being
performed
on the
CREV system
made the A train inoperable.
Work control
instructions
(planning fragnet) required the preferred unit selector
switch to be placed in the
B position.
The control
room operators
subsequently
placed the switch in the
B position.
The inspector
questioned
the effect of the switch being selected to the .A train which
was inoperable.
Logic diagrams
and control drawings were reviewed.
The inspectors
concluded that the
B train of the
CREV would have operated if called
upon.
This was based
on the standby feature design of the two trains.
Since the A train was selected,
an initiation signal would be sent to
both trains to star t, however, only the preferred train would start
immediately.
The non-preferred
system operation would be delayed for
some time by a timer and flow switch arrangement.
If the proper
flowrate is not sensed
in the preferred
system after
a time delay, the
non-prefer red system would start.
The effect of having the A train
selected
would have resulted in the
8 train starting after
a time delay.
The time delay is incorporated into CREV system design.
Therefore,
the
inspectors
concluded that the switch being in the wrong position did not
effect the operability of the
B train.
The inspectors
also questioned
whether the flow switch/time delay
ci rcuitry was periodically tested.
The flow switch is periodically
calibrated.
However, the time delay relay and associated
contacts
have
not been periodically tested
for both trains.
Review of testing of the
system per surveillance instruction O-SI-4.2.G-2,
Control
Room Isolation
and Pressurization
Functional Test,
indicated that the standby feature,
via the time delay and flow switch arrangement,
when the selector
switch
is selected to the 8 train.
has not been tested
since preoperational
testing of the upgraded
CREV system.
The licensee
determined that the
current Technical Specifications did not specifically requi re testing to
be completed;
however, the Improved Standard
Technical Specifications
(ISTS) that the licensee
has submitted for
NRC approval,
require testing
of the control circuit.
The licensee
developed
a work order to confirm
that the
CREVs train A low flow ci rcuitry would start train A when the
system priority selector switch is in the train
B position.
Testing
will be performed
on the requi red periodicity when
ISTS is implemented.
Additional review of the testing
and potential effects of the standby
train logic failures is necessary.
(Unresolved
Item 50-260,296/97-11-03,
Adequacy of CREV Standby Train Circuit Testing)
The inspectors
concluded that the licensee did not adequately
control
the system priority selector
switch. Operating Instruction 0-0I-31,
Control
Bay and Off-Gas Treatment Building Air Conditioning System,
Revision 49, did not have the appropriate
guidance to maintain the
preferred selector
switch in the correct position.
The procedure did
not address
the switch.
Apparently, the procedure
had not been proper ly
~i
0'
02
02.1
revised
when the
CREV system
was modified in 1993.
The inspector also
observed portions of CREVs testing
on December
1,
1997, during which the
operators
had. to reposition the switch without specific guidance.
This
is identified as Violation 260,296/97-11-02,
Failure to Control
CREV
Switch Position.
Conclusion
Procedural
controls were not adequate'to
ensure that the Control
Room
Emergency Ventilation System priority selector switch was maintained in
the correct position.
Additional review is required to determine if
control circuitry in the
CREV system
was adequately tested.
Operational
Status of Facilities and, Equipment
Auxiliar Unit 0 erator
Rounds/Plant
Tours
Ins ection Sco
e
71707
The inspector
accompanied
the Unit 3 rounds
and control bay auxi,liary
unit operators
(AUO) on plant tours.
The inspection
focused
on AUO
thoroughness
and attentiveness
to overall conditions.
The resident
inspectors
also performed
numerous tours to revi'ew plant conditions.
Observations
and Findin s
The inspector
accompanied
the Unit 3 rounds
AUO on November 25,
1997,
and the control bay
AUO on November
29,
1997.
The operators
were
knowledgeable
about current plant conditions
and equipment status.
The
operators
also demonstrated
knowledge of equipment deficiencies
such
as
water leaks.
oi,l leaks, and out of service equipment.
The Unit 3 rounds
AUO also demonstrated initiative and sensitivity to safety system status
by writing a work request
on
a minor Reactor
Core Isolation Cooling
(RCIC) system oil leak identified during,the tour
.
On November 25,
1997, the inspector
observed
local
manual
speed
adjustment of the 3B recirculation
pump motor generator
(MG) set.
The
speed
adjustment
was performed manually to increase plant power
and
balance recirculation
pump speeds.
due to the recirculation
pump
MG set
clutch scoop tube being locked in position because
the speed controller
was not functioning properly.
The evolution was properly supervised
by
a licensed operator.
The operators
properly referenced
and performed
the procedure.
Good communications
and coordination of the evolution
was observed
between the control
room unit operator
and the personnel
performing the speed
change evolution.
The inspector concluded that the
infrequent evolution was performed in a controlled manner.
The inspectors identified that emergency
equipment cooling water
(EECH)
leakage
from the
3B RHR room cooler
.was not being properly collected.
The licensee corrected the problem.
$g~
0
On December
1,
1997. the inspector noted water leakage
from some of the
Unit 3 drywell sandpit
and vent sleeve drains.
The licensee
postulated
that the source of the water
from the drains
may .be from leakage
past
fuel pool cooling valves to the annulus
between the drywell liner and
concrete structure via an overflowing fuel pool liner leakage drain.
The licensee
experienced
water leaking from several
Unit 3 drywell
in February
1997, which may be symptoms of the same
or
a
similar problem.
In addition, during early October
1997, water was
found to be leaking from containment penetrations
for the Unit 3 core
spray
and- the drywell continuous air monitor which could also be
evidence of this problem.
The licensee
documented
the February
1997,
leakage in problem, evaluation
report
(PER) 970400.
,The
PER concluded that the source of the leak
could:not be determined
and that the leak no longer existed.
The
corrective action f'r the
PER was to monitor the penetrations
during the
during the next refueling outage.
The
PER also stated that any further
corrective actions identified by this action item will be added to the
PER by revising the
PER.
The licensee did not document the leakage
identified in October
or December
1997.
Discussions with the licensee
indicated that they were aware of the problem and planned to document
their findings.
Subsequent
to discussions
with the inspectors,
the
li.censee
developed
a troubleshooting
plan to attempt to determine the
cause of the leakage.
The inspectors
also identified that one of the drywell vent sleeve
drains
had no drainage path.
The end of the drain terminates
near the
floor.
Normally the sand pit and vent sleeve drains are cut pipe
ends which would drain to the floor area in the torus
room.
In this
case,
the pipe appeared to penetrate
the floor surface.
The licensee
has initiated
PER 971818 to address
the drainage
path issue.
Conclusion
The local manual
speed
adjustment of the recirculation
pump motor
generator
set
was proper ly supervised
and controlled.
The operators
demonstrated
good communications
and coordination during the evolution.
High sensitivity to safety system status
was demonstrated
by,the
demonstrated
by the Unit 3 rounds
AUO by initiating a work request
on
a
minor RCIC turbine oil leak.
Freeze Protection
Ins ection
Ins ection Sco
e
71714 71707
The inspector
reviewed the. working copy of General
Operating Instruction
O-GOI-200-1,
Freeze Protection Inspection.
Additionally, the, Freeze
Protection
Inspection Discrepancy List and portions of electrical
preventive instructions
EPI.-O-OOO-FRZ001.
FRZ002.
FRZ003 were reviewed.
The inspector also performed walkdowns of the
RHRSW pump rooms
and
channel
diesel fire pump area
and reviewed selected
response
procedures
for freeze protection equipment fai lures.
hl~
0
Findin s and Observations
Review of the working copy of O-GOI-.200-1,
Freeze Protection Inspection,
indicated that the licensee
had appropriately considered
changes
made to
the in-process
procedure since it was initiated.
The revision to the
procedure
included placing space
heaters
into the
RHRSW pump rooms
and
installing tarpaulins
over the
RHRSW pump rooms.
The inspector questioned
the mechanism which initiated the O-GOI-200-1.
Freeze Protection
Inspection procedure.
The licensee indicated'hat
the
procedure
was initiated when the Operations
Periodic Activity (OPA)
database
launched the freeze protection activity on August
1 of each
year.
The 0-GOI-200-1 procedure
requests
that Electrical Maintenance
initiate the electrical preventive i.nstructions
EPI-0-000-FRZ001.
FRZ002
and,
FRZ003.
Implementation of these
procedures
actually began
when the
repetitive preventive maintenance
task form was implemented
on September
3.
1997.
Discussions with the licensee
indicated plans to have the EPI-
0-000-FRZ001,
FRZ002,
FRZ003 procedures
completed
by December
19,
1997.
The inspector concluded that adequate
mechanisms
were in place to prompt
an annual
licensee
review of freeze protection equipment.
The inspector toured the
RHRSW pump rooms
and the channel
diesel fire
,pump area.
Several
areas
were noted in the
RHRSW pump rooms where small
diameter pressure
instrumentation lines had insulation
removed for
apparent
work associated
with the heat tracing.
There were also
examples of larger diameter piping and flange areas
which were not
insulated.
The licensee
had work requests
listed on the freeze
protection inspection discrepancy list which documented
insulation
missing and/or
damaged in each of the four
RHRSW pump rooms.
The
inspector
considered that since the licensee's
freeze protection
inspection
procedures
were implemented in September,
consideration
could
have been given to identifying and correcting problems with small bore
and stagnant
piping as
a priority so that the current configuration of
uninsulated
small bore piping in colder conditions would not have
existed.
The inspector
noted that the licensee's
actions to place
heaters
in and tarpaulins over'the
RHRSW pump rooms provided
a level of
protection for the uninsulated piping.
During the tour of the channel
diesel fire pump, the inspector
noted
that the engine exhaust
pipe was not insulated in accordance
with
drawing 37W215-2,
note 9, which requi red the calcium silicate insulation
to extend through the roof and terminate at the outlet end of the
exhaust pipe.
The drawing note further stated that the insulation
located outside shall
have
an aluminum jacket.
The actual configuration
terminated the insulation on,.the outside of the roof with,an aluminum
jacket,
but the remainder
of the outside pipe run to the outlet end was
not insulated.
The licensee initiated
a
PER to address
the discrepancy.
The licensee's initial review could not determine
a need for the
insulation.
During the inspection period, the inspector
reviewed the Freeze
Protection
Inspection Discrepancy List as maintained
on the Unit 1
ig~
il~
ik
08
08.1
computer.
The inspector noted earlier in the inspection period that
although the
3C emergency diesel
generator
(EDG) room heater
had
a work
request
card written indicating that the room heater would not come on,
the discrepancy
was not identified on the Freeze Protection
Inspection
Discrepancy List.
In addition, the inspector noted the Freeze
Protection Discrepancy List did not indicate if the discrepancy
was
safety related
as suggested
by the procedural
guidelines.
A subsequent
review of the Freeze Protection Discrepancy List noted that the l,icensee
had enhanced
the list to address
whether
the system is safety related or
not.
The
3C
EDG heater
discrepancy
had been
added to the list.
The inspector
compared the
RHR Service Water System Index,
O-SIMI-23A,
f'r 80 instruments
which were listed as Electrical Maintenance
responsible for periodic maintenance
against the electrical preventive
instruction EPI-O-OOO-FRZ001,
Freeze Protection
Program for
RHRSW Pump
Rooms etc.,
Revision 8, to verify that the instruments
were tested.
No
problems were identified.
During the review of freeze protection program electrical preventive
instructions,
documentation errors were identified associated
with
jumper placement/removal
and lead lifts.
No equipment configuration
issues
were identified.
Conclusion
. Adequate
mechanisms
were in place to prompt an annual
licensee
review of
freeze protection equipment.
Small bore and stagnant piping in RHRSW
pump
rooms could have been given priority during inspection
and repair
of freeze protection equipment
so that the identified condition of
uninsulated
small bore piping in colder conditions would not have
existed.
The licensee's
actions to place heaters
in and tarpaulins
over
the
RHRSW pump rooms provided
a level of protection for the uninsulated
piping.
Miscellaneous
Operations
Issues
(92901)
Closed
Violation 260/96-06-02
Failure to Perform
Evaluation Prior to Disablin
.
The inspector
verified that
the revisions to Operating Instruction, OI-55, Annunciator
System,
as
described in the response to the violation dated
September
13,
1996 were
completed.
One of'hose actions
was the completion of safety
assessments
for the annunciators
referenced
in the
The inspector
noted that the reactor vessel
head leakoff annunciator
had been disabled
on October 31,
1997.
With the assistance
of Operations
personnel,
the
inspector obtained
a copy of the safety assessment
performed for this
The assessment
had been completed
on July 31,
1996.
The
inspector
verified that the assessment
adequately
addressed
the aspects
of the annunciator
referenced
in the
The inspector verified that
the requirements
in OI-55 had been
met for disabling the annunciator.
The inspector
noted that this was not the first cycle in which the alarm
was .disabled
and reviewed the licensee's
actions to resolve the issue
causing the problem.
After review of work orders,
examination of the
il~
il
pressure
gage indications,
and discussion with engineering
personnel,
the inspector
concluded that the licensee's
actions to resolve the issue
have been progressive
and reasonable.
The determination that the inner
seal
ring is leaking seems
accurate.
Operation with just the outer seal
ring is described
in the
The licensee
has also listed resolution
of the leaking seal
on the Plant Equipment Action List and is continuing
to pursue resolution.
The violation is closed.
Closed
Violation 260/96-05-03
Customer
Grou
Workers
Exceeded
Overtime Limits Without A
roved
Exem tion.
This violation was
originally discussed
in IR 96-05.
The licensee's
corrective actions
were reviewed.
The inspector
performed
a sample audit of Customer
Group
personnel
work hours during the recent Unit 2 refueling outage.
The
review showed that the proper approvals
were made for overtime hours
which deviated'rom the licensee's
overtime restriction procedure.
The
inspector
also notes that management
stressed,
at plan of the day
meetings during the outage.
the importance for proper approvals for
overtime deviations.
The inspector
concluded that the licensee's
corrective actions were adequate.
The violation is closed.
Conduct of Maintenance
II. Maintenance
Mechanical
Maintenance
Observation
Ins ection Sco
e
62707
The inspector
observed
mechanical
maintenance
work to replace the Unit 1
and
2
B emergency diesel
generator
(EDG) cooling water immersion heater.
Observations
and Findin s
On December
1,
1997, the inspector
observed
mechanical
maintenance
work
to replace the cooling water immersion heater in the Unit 1 and
2
B
emergency diesel
generator.
Discussion with the licensee
indicated that
during troubleshooting to determine the cause of burned lugs in the
control cabinet, testing indicated that problems
may be present with the
immersion heater
even though the heater
appeared to be working.
Mechanical
maintenance
drained the
EDG cooling 'water system
and replaced
the immersion heater coil assembly.
The maintenance
craftsmen
replaced
the coil assembly in accordance
with the step text in work order
(WO)
97-011442-001.
The inspector
noted that the craftsmen
stopped to have
the
WO step text revised when, necessary.
The immersion heater coil
assembly that was
removed
from. the
EDG was found in a degraded
condition.
The decision to replace the immersion heater
coil assembly
was appropriate.
E
il~
il~
il
Conclusions
10
Good mechanical
maintenance
performance
was noted during replacement of
the immersion heater coil assembly
on the
2B EDG.
Effective
troubleshooting to determine the cause of burned lugs in the
EDG control
cabinet identified problems with the immersion heater
even though the
heater
appeared to be working.
Conduct of Engineering
III. En ineerin
Incorrect Hain Steam Pressure
Detectors
Installed in Plant
Ins ection Sco
e
37551
The inspector evaluated
the licensee's
technical operability evaluation
(TOE) performed to evaluate
main steam pressure
detectors with different
upper range limits than specified in the set point and scaling
calculation document.
The inspector also reviewed the licensee's
corrective actions for
an inspector
identified incorrect calibration
frequency calculation for some of the pressure
instruments.
Observations
and Findin s
The inspector
reviewed licensee corrective actions for pressure
detectors installed in the main steam
system which had different upper
range limits than specified in the licensee's
set point and scaling
calculation documents.
A maintenance
worker replacing
a failed pressure
detector identified the condition.
The installed transmitters
were
Rosemount
Hodel
1153GB wi,th a range
code
9 (0-3000 psig) vice the
specified
range
code
8 (0-1000 psig).
One group of the pressure transmitters
detect
main steam pressure
and
input into primary containment isolation system logic to initiate
closure of the main steam isolation valves
on low steam line pressure.
The other group of pressure transmitters
detect turbine first stage
pressure
and input into the reactor protection system to provide
a
signal to bypass the scram protective feature
on turbine stop
or control
valve closure at power levels less than
30K (corresponding with a first
stage
pressure of 154 psig).
The instruments
are not safety related,
however the setpoints
are controlled by TS.
As part of the original design.
selected transmitters
were to be changed
from range
code
9 (0-3000 psig) to range
code
8 (0-1000 psig) using
a
conversion kit.
Subsequently,
a Part
21 notice for this model
transmitter requi red their return to the vendor for maintenance
during
is
11
Unit 2 recovery.
Non-converted transmitters
were sent to the vendor.
Subsequently,
the range
code
9 transmitters
were installed in Unit 2.
A
walkdown of Unit 3 showed that the proper transmitters
were installed.
No violation of regulatory requi rements
occurred since the transmitters
were not safety related.
The licensee
performed
a Technical Operabi.lity Evaluation
(TOE) since
errors
caused
by drift, instrument accuracy,
and ambient temperature
are
dependent
on the upper
range limit of the instrument.
The
TOE
determined that the instruments
were operable.
The inspector
reviewed the site standard
procedure
(SSP)
SSP-12.57.
Engineering Evaluations for Operability Determination,
the Final Safety
Analysis Report
(FSAR), set point and scaling documents,
calculations,
and the applicable vendor manual.
The inspector
found that the
TOE
technically supported
operabi li.ty of the instruments.
The inspector
noted the following deficiencies:
~
The temperature
band
used to calculate the ambient temperature
errors
was different than used in the original calculation.
No
justification for the
new band was provided.
~
Set point and scaling
document information about environmental
ualification and class
(safety related or quality related)
were
ifferent than that specified in the master
equipment list.
~
The original set point and scaling calculation for the main steam
pressure
instruments
analyzed for a calibration frequency of 12
months vice the surveillance instruction requirement of 18 months.
The licensee
subsequently
revised the TOE. the set point and scaling
document,
and the main steam pressure
instrument calculation
based
on
the inspector's
findings.
The discrepancies
did not affect the overall
results of the
TOE or the acceptability of an
18 month calibration
frequency for the main steam pressure
instruments.
A separate
PER was not initially generated
concerning the incorrect main
steam pressure
instrument calibration calculation although the situation
warranted
one.
The inspectors
brought this issue to licensee
management
attention.
Subsequently.
a separate
PER was generated.
c.
Conclusion
Although the technical operability evaluation
was technically
acceptable,
the inspector identified several
deficiencies in the
documented
evaluation.
The individuals involved were reluctant to
generate
a separate
PER concerning
.the incorrect calibration frequency
calculation.
The maintenance
worker who identified the incorrect
installed instruments
demonstrated
a good questioning attitude.
0
0
0
1
Core 0 eratin
Limits Re ort
12
Ins ection Sco
e
37551
The inspector
reviewed the Core Operating Limits, Report for the Unit 2
Cycle 10 operation for compliance with TS.
Observations
and Findin s
Recent
changes to Uni.t 2 TS were made to incorporate the Unit 2 outage
upgrade of the power range neutron monitor instrumentation.
Changes to
thermal limits specifications
were also
made to implement average
power
range monitor and rod block monitor
TS improvements,
and
maximum
extended
load line limit analyses.
The inspector
reviewed the core
operating limits report to ensure
compliance with the revised
TS
requi rements..
No problems were noted.
Conclusions
The inspector
concluded that the licensee properly implemented the Core
Operating Limits Report f'r Unit 2 Cycle
10 in accordance
with the
revised
TS requirements.
Im lementation of Generic Letter
GL 89-10 "Safet -Related Motor-
0 crated
Valve Testin
and Surveillance"
Ins ection
Sco
e
Tem orar
Instruction 2515/109
This inspection provided
an assessment
of the licensee's
implementation
of GL 89-10.
The licensee notified the
NRC that they had completed
implementation of GL 89-10 in letters dated January
9.
1995, for Unit 2
and January
30,
1996 for Unit 3.
In July 1995 the
NRC conducted
an inspection of the
GL 89-10 program and
documented
the results of that inspection in Inspection Report 50-259,
260, 296/95-19.
The inspectors
concluded that the licensee
had
implemented
GL 89-10 for Unit 2 in a satisfactory
manner.
The
inspectors
found that the assumed
values for valve factor,
stem friction
coefficient,
and rate of loading, which the licensee
had used in
determining the settings
and capabilities
for GL 89-10 motor-operated
valves
(HOVs), were .principally based'n
data
from TVA nuclear
power
plants.
The licensee
indicated that it planned to update the data
supporting the assumed
values
and to make adjustments
to the
HOV
settings.
when and where appropriate.
to ensure that the
HOVs were set-
up using correct data.
Additional
HOV testing
and evaluations
were to
be performed to complete implementation of GL 89-10 for Unit 3.
The
licensee's
removal of a number of motor-operated
valves from the scope
of the
GL 89-10 program was observed
and questioned
during the
inspection
and was identified as
an inspector follow up item.
In September
1995 the
NRC conducted
a further inspection of the
program at Browns Ferry, concentrating
on Unit 3.
As documented
in
0
Cl
13
Inspection Report 50-259,
260, 296/95-53,
the inspectors
concluded that
the licensee's
implementation of GL 89-10 for Unit 3 was in the process
of being satisfactorily compl'eted.
The inspectors
were unable to make
a
final assessment.
The licensee
had not completed the testing
and
evaluation of the Unit 3 GL 89-10 program
MOVs.
No Unit 3
HOV test data
were available for inspector
review.
The inspector follow up item
concerning the licensee's
reduction of the
GL 89-10'rogram
scope
remained
open.
The current inspection
was conducted to verify that the licensee
had
satisfactorily completed
implementation of GL 89-10 for both Units 2 and
3.
The principal areas
examined were the previously identified
inspector follow up item regarding
program scope,
the final
HOV switch
setting determinations
and verifications of HOV capabilities established
from the completed testing.
and trending of HOV test
and history data.
The inspection also included
a review of the periodic verification
.
requirements
specified
by the licensee's
GL 89-10 program,
a record
review to verify removal of HOV motor brakes,
and
a plant walkdown to
observe the general
condition of MOVs.
The inspection
was conducted
through
a review of the licensee's
implementing documentation,
interviews with licensee
personnel,
and
observation of MOVs in the plant.
The documents
reviewed included:
o
'VA Nuclear Standard
Department
Procedure
MMDP-5,
"HOV Program,"
Revision 1, dated
September
26,
1997.
o
TVA Standard
Engineering
Procedure
DS-M18.2.21,
"Motor Operated
Valve Thrust and Torque Calculation," Revision 8, dated July 15,
1996.
~
TVA Mechanical
Design Standard
DS-M18.2.22,
"MOV Design Basis
Review Methodology.
Revision
1. dated July 29,
1991.
~
Calculation MD-Q0999-910034,
"NRC Generic Letter 89-10 - Motor
Operated
Valve Evaluation," Revision
13.
o
Other documents
referred to in the following paragraphs.
o
Summary tabulations of MOV information and calculation results
prepared
by the licensee.
Prominent
among the tabulations
referred to above
was
a list of
"available valve,factors"
(AVFs) for the licensee's
GL 89-10 gate
and
The AVFs were calculated
using formulas described in
revious inspection reports
(e.g.,
Inspection Report 50-338,
339/97-01).
he inspectors
compared the AVFs for the licensee's
HOVs to
valve factor requirements
established
in industry testing which the
NRC
had previously reviewed.
These
comparisons
were performed to determine
if the licensee's
AVFs were reasonable.
0
0
4l
b.
Observations
and Findin s
14
1.
Sco
e of MOVs Included in the
GL 89-10 Pro ram
A reduction in the scope of MOVs included in the Browns Ferry GL 89-10
rogram was questioned
during Inspection 50-260,
296/95-19.
The
icensee
had reduced the scopes for Units 2 and
3 from 56
MOVs each to
36 MOVs each,
based
on a re-evaluation -of the functions of the
MOVs.
This reduction in scope
was identified for further review as Inspector
Follow up Item (IFI) 50-260(296)/95019-01,
Reduced
Scope of Valves in GL 89-10 Program.
In a letter dated
October
7,
1996. the
NRC informed the licensee that it
had concluded that the criteria used
by TVA in re-evaluating
the safety
functions of the Browns Ferry
MOVs were unsatisfactory
and
may have
resulted in inappropriate
removal of MOVs from the Browns Ferry GL 89-10
rogram.
An assessment
for the valves
removed
was enclosed with the
etter.
The
NRC requested
the licensee to re-examine the safety
functions of the Browns Ferry
HOVs consistent with the
NRC assessment
and to provide any appropriate corrections
to the
GL 89-10 program.
The
licensee
was asked to notify the
NRC of the findings of the re-
examination
and the actions taken
as
a result of those findings.
In a letter dated January
6,
1997. the licensee
provided
a response to
the NRC's request for re-evaluation of the safety functions of the
removed from, or not included in, the Browns Ferry GL 89-10 program.
The licensee
stated that
15
MOVs were being added to the individual
GL 89-10 sub-programs
for Units 2 and 3.
The licensee
also stated that
plant procedures
were being revised to require that the applicable
system,
or train, for 18
MOVs (per unit) be declared
inoperable if the
valve was taken out of its normal (i.e.. safety) position for testing.
The licensee
noted that the applicable
Browns Ferry Technical
Specification Limiting Conditions for Operation would govern until such
testing
was completed
and the valve was returned to its normal position.
The letter identified the involved
MOVs and the dates
when these
commitment actions would be implemented.
The addition of 15 valves to
each unit's sub-program
was to be completed
by January
31,
1997.
The
procedure
changes
regarding operability during testing f'r 18
MOVs were
to be completed
by February
21,
1997.
During this inspection,
the inspectors verified that the 15
MOVs listed
in the licensee's
letter of January
6.
1997,
had been included in the
GL 89-10 sub-programs
for Browns Ferry Units 2 and 3.
The GL 89-10 sub-
programs for Units 2 and 3 at Browns Ferry each contained
34 gate valves
and
17 globe valves.
The inspectors
reviewed
a sample of the related
licensee's
procedures
to determine whether the associated
system or
train would be declared
when any of the identified 18 MOVs
were placed in their non-safety positions.
The inspectors
found that
the licensee fai'led to provide the appropriate
procedural
requi rements
for several
MOVs.
For example,
Surveillance Instruction (SI) 3-SI-
4.5.B. l.c(II), Revision 9, did not declare Unit 3
RHR Loop II inoperable
when
MOV 3-FCV-74-66 was cycled.
Similarly, SI 2-SI-4.5.B.l.c(II),
Revision 21, did not declare Unit 2
RHR Loop II inoperable
when
MOV 2-
FCV-74-66 was cycled.
The licensee's
failure to revise plant procedures
in accordance
with its January
6,
1997 letter is
a deviation from a
commitment (260,296/97-11-04).
2.
Determinations of Settin
s and Verifications of MOV Ca abilities
'I
Switch Settin
s
The licensee controlled the operation of MOVs in its GL 89-10 program
.
through
a combination of torque
and limit switches.
The torque switch
was bypassed
in the closing di rection for 95 to 98K of stroke length as
confirmed
by diagnostic data.
For opening,
the torque switch was
bypassed
for the entire stroke.
The licensee calculated the thrust and torque requirements
for MOVs in
the
GL 89-10 program using standard
industry equations.
The predicted
thrust requirements
for gate valves were calculated typically assuming
a
.0.4 valve factor with a 20K safety factor .
For globe valves,
the
licensee
assumed
a valve factor of 1.0 for closing and 1.2 for opening.
The licensee typically assumed
a stem friction coefficient of 0. 15 and
margin for potential
reduction in thrust output under
dynamic conditions
(referred to as rate of loading) of 10K for gate valves
and
15K for
'For MOVs with roller-screw stem nuts, the licensee
based
the stem friction .coefficient on manufacturer's
information.
Oiagnostic
error and torque switch repeatabi lity were accounted
for in the switch
setting cal'culations.
The licensee established its assumptions
for
determining predicted thrust
and torque requirements
based
on test data
principally from Browns Ferry and other
TVA nuclear
power plants.
The inspectors
noted that thrust settings for a few MOVs at Browns Ferry
had .not been
updated in the controlling setting drawings to reflect the
results of the dynamic tests
performed earlier in 1997.
The licensee
acknowledged that its
MOV setting drawings
needed to be updated.
Accuracy of the
MOV setting drawings will be re-evaluated prior to the
NRC closing its review of the Browns Ferry GL 89-10 program.
For some
MOVs, the licensee
assumed
run efficiency in the closing
direction when predicting the torque output capability of its actuators.
The inspectors
noted. that the actuator manufacturer
is preparing
new
guidelines that might affect the acceptability of the licensee's
use of
run efficiency.
Licensee
personnel
stated that they were aware of this
situation
and would address
the capability of the affected
MOVs when the
new guidance
was issued.
Oesi n-Basis
Ca abilit
At Browns Ferry, the licensee
had dynamically tested
8 gate valves
and
7
globe valves in Unit 2,
and
5 gate valves
and
7 globe valves in Unit 3
16
as part of its GL 89-10 program.
The test data for each of these valves
was used to establish its valve factor,
stem friction coefficient,
and
rate of'oading.
Using these,
the calculations
and settings
for. each of
the dynamically tested
valves were revised.
For
MOVs tested at partial design-basis
differential pressure
conditions,
the licensee extrapolated test data
from test conditions to
design-basis
conditions in evaluating thrust
and torque requi rements.
Appendix
E of MMDP-5 provided guidelines for in-plant differential
pressure testing of MOVs at Browns Ferry.
The inspectors
noted, that the
guidelines did not clear ly address test conditions that would provide
sufficient contact load to assure reliable data.
The inspectors
did not
identify any cases
where this resulted in unsatisfactory
data.
The
licensee
agreed that clarification was appropriate
and indicated that
additional
guidance for test setup conditions,
such
as prepared
by the
Electric Power
Research
Institute, would be provided to ensure reliable
extrapolation of dynamic test data.
For the non-dynamically tested
valves,
Browns Ferry still relied on the
general
valve factor assumptions
(e.g..
0.4 for gate valves) established
by the licensee's
corporate office for determining the predicted thrust
and torque requi rements.
It had not formally assessed
the validity of
these
assumptions
based
on test information.
The inspectors
found that
some of the results
from tests
performed at Browns Ferry did not support
the assumptions.
For example.
dynamic tests
completed at Browns Ferry
in 1995 (subsequent
to previous
NRC GL 89-10 inspections)
on
MOVs 3-FCV-
75-09,
3-FCV-75-37,
and 3-FCV-74-71 revealed
gate valve factors of 0.6
or greater.
The inspectors
also noted that the licensee
had not
performed
a documented
evaluation of the test data to verify the
adequacy of the program assumptions
for stem friction coefficient and
rate of loading effects.
The licensee's
fai lure to evaluate
dynamic
test data in relationship to its
GL 89-10 program assumptions
could have
resulted in MOVs being incapable of performing their safety functions.
The inspectors
found that the issue of the licensee's
failure to assess
the validity of its assumptions,
as discussed
in the preceding
paragraph,
had been identified in a licensee
self-assessment
conducted
in May 1997.
In the self-assessment
report dated
November 7,
1997, the
licensee
determined that the Browns 'Ferry GL 89-10 program was not
adequate
to support
an
NRC inspection of GL 89-10 implementation.
One
of the recommendations
in the self-assessment
report was that
justifications and analyses
were needed to strengthen
the basis for the
assumed
valve factor and other appropriate factors.
This was identified
for. resolution in Browns Ferry Problem Evaluation Report
(PER)
971770
(initiated on November
12,
1997).
The
PER stated that the licensee's
corporate
engineering office had issued
a white paper that concluded
that
a valve friction factor of 0.6 should
be used for gate valves that
could not be dynamically tested.
The
PER also indicated that the valve
factor guidance provided in Design Standard
DS-M18.2.21
was inadequate
and that .an evaluation of the
MOVs in the
GL 89-10 program was required
to ensure the abi'lity of these
MOVs to perform their safety functions.
Using
a valve factor of 0.6 for gate 'valves
and 1.2 for globe valves,
'
0
17
the licensee
reviewed the capability of its GL 89-10
MOVs to perform
.their safety functions.
In some cases,
the licensee relied on actual
dynamic test data
or bypass of the torque switch to justify the
operability of'ts
MOVs.
The licensee
was currently completing its
plans for justifying the design assumptions
for valve factor,
stem
friction coefficient and rate of loading effects.
In a letter dated
December
15,
1997. the licensee indicated it would revise its GL 89-10
program by January
30,
1998, to address
issues
such
as the adequacy of
the design assumptions.
The inspectors
considered
the licensee's
failure to evaluate test data to assess
its GL 89-10 program design
assumptions
to be
a violation of the requi rements of 10 CFR 50 'ppendix
B, Criterion III, "Design Control."
The inspectors verified that the
violation was not repetitive.
This non-repetitive,
licensee-identified
and corrected violation is being treated
as
a Non-Cited Violation,
consistent with Section VII.B.1 of the
260,296/97-11-05).
Another example is identified in a subsequent
paragraph of this report section.
The inspectors
found that the licensee
had incorrectly evaluated
the
operability of'everal
MOVs in Problem Evaluation Report
(PER)
940066
(initiated on March 22,
1994).
In the evaluation,
the licensee
had
relied on the "stall efficiency" of MOV actuators to evaluate the
operability of the
MOVs.
The actuator
manufacturer
had provided
a value
for stall efficiency for'se by licensees
in evaluating potential
structural
damage in the event of an actuator
motor stall condition.
The manufacturer,
Limitorque, specifically stated that the use of stall
efficiency .was not reliable for predicting actuator output capability.
For example,
see Limitorque Haintenance
Update 92-1 (issued in 1992) or
Application Guide for Motor-Operated
Valves in Nuclear
Power Plants,
(NP-
6660-D, dated
March 1990) prepared
by the Electric Power
Research
Institute.
A current evaluation using the appropriate efficiency showed
that the valves
had been operable..
However, the inappropriate
use of
stall efficiency in predicting actuator output could have resulted in
the licensee
not recognizing
an inoperable condition of a safety-related
MOV.
The inspectors
considered
the licensee's
use of stall efficiency
to represent
a violation of the requirements
of Criterion III of 10 CFR 50, Appendix B, Design Control.
The inspectors
found that the licensee
had recognized that use of stall efficiency .was inappropriate
and that
evaluations
subsequent
to
PER 940066 did not use stall efficiency.
For
example,
the licensee
evaluated the operability of its GL 89-10
MOVs in
its recent
PER 971770 using pullout or run efficiency (rather
than stall
efficiency) together with consideration of the applicable motor curves.
The inspectors verified that the"violation was not repetitive.
This
non-repetitive,
licensee-identified
and corrected violation is being
treated
as
a Non-Cited Violation, consistent with Section VII.B.1 of the
NRC Enforcement Policy (50-260,296/97-11-05).
Another example is
identified in a preceding
paragraph of this report section.
0
0
0
MOV De radation
18
The inspectors
found that the licensee
had not provided clear guidance
for addressing
potential degradation of HOV performance.
The licensee
agreed that its guidance could be clarified and initiated steps
for this
action.
3
M~QV T
di
GL 89-10 suggested
that
MOV data
on failures
and corrective actions
(including repairs,
analyses,
as-found deteriorated
conditions, etc.)
be
periodically examined at least every two years or after each refueling
outage to establish
trends in MOV operability.
Currently, the licensee
implemented this trending through requi rements in Procedure
MHDP-5.
Until'evision 0 of MMDP-5, became effective on August 20.
1997, the
trending requirements
were specified
by Site Standard
Practice
SSP-6.51,
"Program Plan for Generic Letter 89-10," Revision 3
~ effective January
10,
1996.
MMDP-5 requi red issuance of an
MOV trending report at the
completion of every testing cycle (18 months or end of each refueling
outage).
The report was to include (1)
MOV signature analysis report
and (2) maintenance
history (corrective
and preventive).
SSP-6.51
had
required
a similar report at the same periodicity.
The inspectors
found
that the licensee
had not prepared the trending report required
by the
rocedures.
The licensee's
failure to prepare the trend report required
y procedures
is
a violation of 10 CFR. 50. Appendix B, Criterion V,
"Procedures"
(50-260,296/97-11-06).
4.
Periodic Verification of MOV Ca abilit
In Section 3. 13 of MMDP-5, the licensee stated that the purpose of
periodic monitoring of MOVs was to ensure
continued
MOV ability to
function under
design-basis
conditions,
and to identify isolated or
generic problems with MOVs or the overall program.
MNDP-5 also noted
that periodic verification should identify deterioration of MOV
components
before significant degradation
occurs.
MMDP-5 indicated that
the licensee
was working with the owners groups to share test data.
In
a letter to the
NRC dated
March 17,
1997, the licensee stated that it
was participating in a joint owners group program in response to GL 96-
05, Periodic Verification of Design-Basis Capability of Safety-Related
Motor-Operated
Valves.
The licensee's
plans for MOV periodic
verification were found to be adequate for GL 89-10.
The
NRC may re-
assess
the licensee's
long-term
MOV periodic verification program as
part of its review for GL 96-05.
I
5.
Walkdown
The inspectors
conducted
.a plant walkdown of MOVs to- assess
their
condition.
A previous walkdown described
in Inspection Report 50-259,
260, 296/95-53,
reported that cover bolts were loose or missing
on
several
MOVs.
The inspectors
did not observe
any similar examples
during the current inspection.
The inspectors
noted
a significant
difference in the quality of stem grease
applied to various
MOVs. This
0
1
0
19
was apparently
due to the licensee's
past
use of different stem greases.
A future closeout inspection for GL 89-10 will examine whether the
licensee's justification of'tem friction coefficient and rate of
loading effects are applicable to the different greases
or a possible
mixture of the greases.
The inspectors
al'so observed the presence of a
plastic cap
on an actuator
grease relief line for one
HOV (2-FCV-74-
106).
This was not
a
HOV.
The licensee
acknowledged
the
inspectors'alkdown
findings and stated that appropriate action would
be taken.
6.
Motor Brakes
Inspection
Report 50-259,
260, 296/95-53 indicated that motor brakes
had
not been
removed from HOVs 3-FCV-73-34, 40,
and 44.
During the current
inspection,
the inspectors
reviewed documentation
attached to BFPER
940038 which verified that the brakes
had been
removed.
c.
Conclusions
Implementation of GL 89-10 at Browns Ferry was not sufficiently
developed to permit the
NRC to complete its review.
The inspectors
did
not identify any immediate operability concerns with GL 89-10 .HOVs at
Browns Ferry.
The inspectors
identif'ied a violation involving the licensee's
failure
repare
a trend report required
by procedures
and
a deviation from a
icensee
commitment to revise procedures
to assure
the applicable
system
or train for certain
HOVs would be declared
when the
were placed in thei r non-safety positions during operation.
In
addition,
a non-cited violation resulted
from (1)
a failure to evaluate
HOV test data to verify that it supported
GL 89-10 program design
assumptions
and (2) improper use of actuator stall efficiency.
A summary of the principal actions to be performed
by the licensee to
address
the issues identified in this inspection
and complete
implementation of GL 89-10 is as follows:
Preparation of test-based
justifications for the valve factor,
stem friction coefficient,
and rate of loading assumed
in the
design calculations for each
HOV (including MOVs with
special
features
such
as roller screw stem nuts, different stem
greases.
or mixed stem greases).
(Refer to NCV 50-260,296/97-11-
05)
Updating of calculations
and
HOV setting drawings
based
on the
justified assumptions.
Implementation of trend reporting based
on the periodic reviews
recommended
by GL 89-10.
(Refer to VIO 50-260,
296/97-11-06)
E2
E2.1
20
~
Correction of procedures
that did not implement the licensee's
commitment to assure that the applicable
system or train for
certain
HOVs would be declared
when the
HOVs were
placed in their non-safety positions during operation.
(Refer to
DEV 50-260.296/97-11-04)
In a letter
dated
December
15.
1997, the licensee
committed to revise
the Browns Ferry GL 89-10 program by January
30,
1998, to address
the
design input issues identified during this inspection.
Further, the
licensee
committed to revise its
MOV design ca1culations to reflect the
GL 89-10 program design input revisions
by Harch 31,
1998, for Unit 3,
and August 31.
1998, for Unit 2.
The
NRC will re-inspect the
program at Browns Ferry following notification from the licensee that
the issues
described in this report are sufficiently resolved to permit
verification that the intent of GL 89-10 has
been met.
The licensee
stated that
a status letter would be provided to the
NRC by March 2.
1998, indicating its progress
in completing the commitment actions.
Engineering
Support of Facilities and Equipment
Unit 2 Reactor
Due to
EHC Leak and Reactor
Protection
S stem Rela
Problem
Ins ection Sco
e
37551
93702
The inspectors
monitored
and reviewed the licensee's
investigation
and
corrective actions following a Unit 2,reactor
Observations
and Findin s
After the Unit 2 reactor
on October 28,
1997, the licensee
appointed
an Incident Investigation (II) team headed
by an engineering
manager to determine the cause of the scram.
Some initial information
indicated that
pressure
problem was involved.
Later
on October
28, the licensee
simulated the same conditions which existed
when the scram was received
and inspected
the air system.
No problems
were found.
The low pressure
was subsequently
determined to have
occurred after the scram
as expected.
The inspectors
reviewed
information relating to previous
which supported the conclusion
that the scram air system
had performed
as expected.
The investigation continued
and early on October 29. the II team
developed
a postulated
cause of the scram.
Additional troubleshooting
and, diagnostic testing enabled the team to conclude the following
sequence
of events
associated
with the scram:
A half scram was present
on the A side of the Reactor
Protection
System
(RPS)
due to the g1 turbine control valve (CV) being closed
for repair of an electrohydraulic control fluid leak.
The 5A-K14B relay, associated
with the Bl RPS ci rcuitry,
unexpectedly
de-energized.
The team found this through
a detailed
0
0
21
review of computer information involving relay conditions at the
time of the scram.
The 5A-K14B relay has contacts
in the
circuitry which serve to de-energize
some of the scram solenoid
ilot valves
(as well as other functions). It is located at the
ottom of a long sequence of normally shut contacts,
any of which
open to initiate
a scram signal.
Two of those contacts
are from
one
GE HFA relay connected to the
CV fast closure circuitry which
senses
CV closure
as
a function of EHC pressure
at the valve.
The
parallel relay (5A-K14F) in the Bl RPS circuitry did not de-
energize.
The licensee
performed testing which showed that,
on
decreasing
voltage, the 5A-K14B relay contacts
began to chatter or
cycle at
a voltage value above that at which the relay (and the
5A-K14F relay) de-energized.
The 5A-K14B relay which is
a
CR105
was replaced
and tested.
The relay will be examined
for more information on the failure mechanism.
The other
solenoid pilot valve relays were also tested
and no others
were
found to display the characteristics
seen
on the 5A-K14B.
The licensee
also conducted cycling of the turbine control valves
and monitored pressure
indications at the point that
a turbine
control valve fast closure signal
(decreasing
EHC pressure)
would
be sensed.
The testing
showed that cycling of the valves
caused
notable
(300-400 psig)
downward spikes in
EHC fluid pressure.
Subsequently,
the licensee
indicated that modification of the
'ystem to reduce these osci llations (installation of orifices) was
being considered.
~
Despite testing,
the licensee
did not find any problem with the
turbine fast closure relay which has two contacts in the Bl RPS
circuitry to the 5A-K14B relay.
It is postulated that the
momentarily sensed
decreased
EHC fluid pressure
caused the relay
contacts to open just long enough to de-energize
the sensitive
5A-
K14B relay.
~
The conditions resulted in about half of the Unit 2 SSPVs getting
an "electrical" scram signal
(channel
A t, scram
and the one relay
in the Bl channel).
This would cause the Group I and
IV rods to
get
a scram signal.
This theory also conforms with an Senior
Reactor Operator's
(SRO) observation that the Group I and
IV rod
groups
scram lights appeared to have actuated
before the other two
groups.
~
A "8" RPS side backup scram valve was energized
by, the 5A-K14B (in
conjunction with the half scram) which vented air off of the
control rod drive air header
and
a full scram was actuated.
The resident
inspectors directly observed portions of the
troubleshooting
and corrective actions.
Workers replacing the 5A-K14B
relay were attentive in their work and were utilizing good stop-think-
ask-and-act
techniques.
The inspectors
examined recorder
traces
which
supported
the licensee's
conclusions
regarding
EHC fluid pressure
oscillations
and relay performance.
Portions of testing of some of the
0
22
other
RPS relays were observed.
The inspectors
noted that the pressure
switches set point for turbine fast closure input to RPS were
conservatively
above the value specified in the Updated Final Safety
Analysis Report
(UFSAR).
One of the inspectors
attended
the restart Plant Operations
Review
Committee meeting
and noted that the II team
made
an effective
presentation
regarding the electrical
equipment
performance which caused
the scram.
The inspector
questioned if General Electric
(GE) had any
additional information regarding the
EHC pressure
spike theory and the
parallel
RPS relays not being actuated.
At the time, it was not known
if additional information was available,,but
management
indicated that
it was being pursued.
The II team also
recommended
several
long term
action items including development of stronger procedural
guidelines for
repairs of a control valve servo while at power.
Prior to restart,
the
licensee tested the other scram contactors
and did not identify any
problems.
A few days later,
a
GE engineer
noted that Service Information L'etter
(SIL) 508,
Scram Contractor Coil Life and Maintenance,
addressed
a
similar issue.
The SIL was issued in February
1990 and addressed
an
unexpected
scram at another Boiling Water
Reactor
which had been
caused
by some scram contactors
dropping out during very short duration scram
signals.
The inspector obtained
a copy of the SIL and the licensee's
documented
actions in response to the SIL.
The circumstances
involved
in the scram described
in the SIL appear to be very similar to the
Browns Ferry scram.
The SIL recommended that preventive maintenance
be
performed in the contactors
and that thei r service life be reviewed.
Documentation indicated that the Browns Ferry Unit 2 scram contactors
had been replaced in 1988 and thus would not be expected to be
approaching
end of service life.
The inspector
reviewed portions of
Procedure
EPI-099-RLY001,
and concluded that it addressed
the preventive
maintenance
recommended
in the SIL.
Licensee
Event Report
was submitted to the
NRC on
November 25,
1997,
and addressed
the scram.
The
LER included
description of corrective actions to reduce
EHC pressure
decreases
during control valve movement through
EHC system modifications.
After startup of the unit, several
other incidents of control valve
servo leaks occurred
on Unit 2.
(A total of six servo leaks occurred
on
Unit 2 since startup after the refueling outage).
The leaks were
identified through careful monitoring of the
EHC tank levels.
In each
case,
power
was reduced
and the servos
were replaced.
The licensee
revised the repair
procedures
to include recommendations
from the II
team.
The inspector s verified that TS requi rements
were met during the
work activities which included installation of jumpers around pressure
switches with inputs into the Reactor
Protection
System.
The licensee
formed
a team which continued to investigate the cause of
the leaks.
The investigation included extensive testing of postulated
causes
and working with the servo vendors.
Subsequently,
the licensee
0
4i
23
determined the leaks were due to vibration or pressure oscillation
induced
movement of a servo port plug which was not secured sufficiently
to prevent the movement.
The plug movement
(a few mils) resulted in
degradation of an o'ring seal
and consequently
EHC oil leaked out of the
servo.
The leaking servos
had been replaced during the most recent
refueling outage with rebuilt servos.
The licensee indicated that the
servos
are rebuilt by two vendors which utilize different means of
securing the plug.
The plugs
on the leaking servos
were secured
in a
manner that .appeared to allow slight movement of the plug.
.At the close
of this report. the licensee
was attempting to procure replacement
servos of the type which seem to allow less plug movement.
For the
interim period, the licensee
has revised work instructions for servo
replacement
such that the plug will be more securely fastened.
Unit 3
also has the same type of servos installed but no leakage
has
been
detected.
Those servos apparently were from a different batch than the
Unit 2 servos.
The licensee is continuing to investigate the magnitude
and significance of vibrations .in the Unit 2
EHC system.
Work
instructions
have been
developed to install
a pressure
transducer
on
a
Unit 2 control valve during the next replacement that is performed.
The
device will monitor
EHC fluid pressure
at the control valves.
Problem Evaluation Report
(PER) 971714 described
the investigation
and'orrective
actions
regarding the
EHC leaks.
The
PER noted that
additional
EHC system modifications. including installation of
and control valve manifolds,
are planned
as part of the
Power Uprate Project.
These modifications are referenced
in GE Turbine
Information Letter 1123,
issued
November
14,
1992.
The modifications are
intended to reduce
EHC fluid pressure oscillations.
Operations is
continuing to closely monitor
EHC reservoir fluid level
on both units.
The inspectors verified that the enhanced
monitoring is being properly
performed.
Conclusions
The inspectors
concluded that the l.icensee's
incident investigation
team
performed well in investigating the equipment
issues
which caused
the
The team studied available
information, developed
a theory of
the cause,
and in a prompt manner,
performed electrical testing which
supported the postulated
cause.
The investigation into the
EHC fluid
leaks
was also thorough
and determined the cause of the leaks in a
reasonable
time, period.
Levels Increased
Ins ection Sco
e
37551
The inspector
reviewed data
and developed
a time line to assess
the
licensee's
actions in response to -high particulate levels in the Reactor
Core Isolation Cooling (RCIC) system lube oil.
Oil samples
indicated
a
articulate count which was in the action range
as identified by the
icensee's
procedures
and documentation in the vendor manual.
l
b.
Observations
and Findin s
24
On October 20.
1997,
a lube oil sample
was taken from the
RCIC system
following work which had been performed during the Unit 2 outage which
ended October
18,
1997.
Oil analyses
results
were issued
from the
licensee's
Central
Laboratory on October 22,
1997, which identified
a
particulate count of ISO 20/15.
On November 3,
1997, the licensee initiated a work request
C337743 to
sample the oil again to verify the high particulate content
and change
the oil if necessary.
On November 6,
1997, the sample
was taken to
verify Central
Laboratory results.
Browns Ferry laboratory determined
the particulate count,to
be high and that
an oil change
was required.
On November 21,
1997, the licensee
changed the oil in the
RCIC system.
Sampling following the oil change indicated
a high level of particulate.
The licensee
changed the oil and sampled for particulate levels several
times in an, attempt to decrease
particulate levels to within the normal
range.
Analyses of the oil sample taken from the RCIC system following
a 15 minute run on November 23.
1997,
showed
a particulate level of ISO
18/14 which placed the system in the Alert Range.
The Alert Range
requi res that the lube oil be filtered or replaced at the next refueling
outage if the alert limits persist.
On November
23,
1997, the licensee
declared the RCIC system operable.
Chemistry Instruction (CI) CI-130, Diesel
Fuel
and Lube Oil Monitoring
Program,
Revision
5
~ Attachment 3, describes
particulate guidelines.
The procedure
describes
three ranges:
Normal
Range
(ISO 16/13), Alert Range
(ISO 18/15),
and Action Range
(ISO
>18/>15).
The procedure states that the particulate counts which exceed
the alert range require immediate corrective action to be taken to
restore the oil to normal or alert levels.
The procedure further states
that the HPCI/RCIC system
may remain "functional" for a period not to
exceed
30 days while resampling / filtering / replacement activities are
in process.
The licensee
interpreted the procedural
requirements to
mean that the oil should
be changed within 30 days.
The RCIC,oil was
changed within thirty days of the date when the oil analysis results
were issued
from the licensee's
Central
Laboratory on October 22.
1997.
The licensee is in the process of developing guidance for the lube oil
program on site.
In inspection report 259,260,296/97-08.
the inspector
concluded that
weaknesses
in the licensee's
lubrication oil analysis
program permitted
the incorrect type of lubricating oil to be added to a second
several
months af'ter it had been installed in a different
EDG.
c.
Conclusions
Al.though the licensee's
actions to decrease
the oil particulate levels
in the
RCIC system were adequate,
the
RCIC oil particulate level issue
represents
another
example of the difficulties that the licensee is
II
E8
E8.1
25
experiencing with the lube oil analysis
program.
The licensee
has not
determined the cause of increased particulate but has determined it is
not due to excessive. bearing wear.
Miscellaneous
Engineering
Issues
(92902)
Closed
Ins ection Fol,low u
Item 50-'260 296/95-19-01:
reduced scope'of
valves in GL 89-10 program.
This item involved the licensee's
removal
of a number
of. valves from its GL 89-10 program.
The licensee's
actions
to resolve this item are discussed
in E1.3.b.1
above.
The licensee's
.
actions in returning valves to its program were satisfactory,
except
as,
addressed
by the violation described in that section of this report.
R2
R2.1
IV.
Plant
Su
ort
Status of Radiation Protection
and Chemistry Facilities and Equipment
Radi oacti ve Effluent Honitor Probl ems
Ins ection Sco
e
37551
71750
During review of operating logs, the resident inspectors
had noted
discussion of a problem involving the radioactive effluent monitor (0-
RH-90-130).
The inspector
questioned
resolution of the problem and the
'bsence
of a Problem Evaluation Report at
a subsequent
Management
Review
Committee
(HRC) meeting.
Several
days later, the problem occurred
again.
The inspectors
questioned
plant management
regarding the
problems
and the oper abi:lity status of the monitor .
The licensee
formed
an investigation team.
The inspectors
reviewed the regulatory
and
procedural
requirements
for the monitor,
examined the detector
and
associated
piping,
and monitored the licensee's
investigation.
b. Observations
and Findin s
The resident inspectors
noted that the October 21,
1997. operating
logs
described
an incident in which the radwaste
operators
had secured
an
effluent release after it was noted that the radiation monitor was
indicating an activity level which dropped to less than the background
level recorded before the release
began.
In accordance with the Offsite
Dose Calculation Manual, the monitor is required to normally be operable
during releases.
Releases
are permitted to be continued with an
inoperable monitor if compensatory
measures
are completed.
The release
was subsequently
restarted.
At a Management
Review Committee meeting,
the resident inspector questioned
the
resolution of the problem and .the
.absence of a Problem, Evaluation Report
(PER).
Subsequently,
maintenance
personnel
reported to the inspector that the problem had been attributed
to demineralized water remaining in the detector after
a cleaning
evolution.
C
0
26
On October 27, the problem occurred again.
The monitor was not declared
and two releases
were made without compensatory
sampling
performed.
PER 971713 was initiated on October
28 to address
the issue.
After HRC review of this
PER on October 29. the inspector
questioned
the
operability status
of. the monitor since releases
were being
made without
completion of compensatory
measures
required
by the Offsite Dose
Calculation Manual
(ODCH).
The inspectors
also questioned
plant
management
regarding resolution of the problems.
The monitor was
declared
inoperable (administrative decision)
on October
29 and
compensatory
measures
were completed for all releases.
An Incident
Investigation (II) team was formed .to investigate the problems.
After some investigation,
the team identified that the problem was
caused
by water leaking out of the detector
housing
volume through
a
closed drain valve.
Maintenance
personnel
found an accumulation of crud
on the valve seat which allowed leakage
through the valve.
Drainage of
water out of the volume decreased
the shielding between the detector
and
the chamber walls.
When
a release
was started,
the volume was refilled
with low activity water and the radiation levels sensed
by the detector
wer e reduced.
The valve was replaced. and the licensee
subsequently
conducted testing .which supported
the postulated
cause.
During a
subsequent
release,
the decreased
radiation levels were not observed.
The investigation
team concluded that the RH-130 monitor had, in fact,
been functional despite the water draining problem.
The team also
verified that the
ODCM compensatory
measures
had been completed for all
periods in which the monitor had been inoperable.
The inspectors
reviewed portions of Technical
Instruction O-TI-45, Liquid Process
Radiation Monitors.
This procedure
determines
the alarm setpoints
as
required
by the
ODCH.
At Browns Ferry, 'liquid radwaste
batch discharges
are controlled by procedure O-SI-4.8.A, Liquid Effluent Permit.
Representative
samples
are analyzed prior to the discharge
and the
monitor serves
as
an independent
check during the discharge.
The
inspectors
noted
numerous
conservatisms
were applied, in the set point,
determinations
for 'RH-130, including conservative
assumptions
regarding
condenser circulating system (dilution) water flow.
After review of the
procedures
and discussions
with the team, the inspectors
concluded that
the decreased,
background effects observed
did not adversely affect the
.operability of the monitor.
On December
2,
1997, the .proposed corrective actions for
PER 971713 were
reviewed, by the Management
Review Committee
(HRC).
Initially, the
actions did not address
the inspector's principle concern that observed
abnormalities
associated
with the RM-130 were not fully understood
and
radioactive material
releases
were permitted to continue without
compensatory
measures.
During the
HRC meeting, the Site Vice President
directed that
a corrective action
be added which addressed
this concern.
The inspector discussed
the concern with the Operations
Manager
and
verified that the concern would be adequately
addressed.
\\
ll
0
c.
Conclusions
27
Unexpected indications
on the radioactive effluent monitor
recorder
were
not thoroughly investigated prior to discontinuation of compensatory
actions
required for an inoperable monitor.
The licensee
subsequently
completed
a detailed
investigation which identified that
a leaking
valve had caused
the unexpected
indications.
The investigation also
concluded that the monitor was not inoperable
and that regulatory
requirements
were met during, the period.
Xl
Exit Meeting Summary
V.
Mana ement Meetin s
The resident inspector presented
inspection findings and results to
licensee
management
on December
12.
1997.
Other formal meetings to
discuss
report issues
were conducted
on November
21,
and
December
3,
1997.
The licensee
acknowledged
the findings presented.
Proprietary
information is not included in this inspection report.
PARTIAL LIST OF
PERSONS
CONTACTED
T. Abney, Licensing Manager
J. Brazell, Site Security Manager
R. Coleman, Acting Radiological Control
Manage
M. Cooper,
Corporate
Component
Engineering
Manager
J.
Corey, Radiological Controls
and Chemistry
Manager
T. Cornelius,
Emergency
Preparedness
and Planning
C. Crane, Site Vice President,
Browns,Ferry
R.
Greenman,
Training Manager
J.
Johnson,
Site Quality Assurance
Manager
R. Jones,
Assistant Plant Manager
G. Little. Acting Operations
Manager
D.
Nye, Site Engineering
Manager
J. Schlessel.
Acting Maintenance
Manage
K. Singer,
Plant Manager
INSPECTION
PROCEDURES
USED
IP 37551:
IP 40500:
IP 62707:
IP 71707:
IP 71714:
IP 71750:
Onsite Engineering
Licensee Self-Assessments
Maintenance
Observations
Plant Operations
Cold Weather Preparations
Plant Support Activities
0
(
0
0
IP 9Z901:
IP 92902:
IP 93702:
TI 2515/109:
28
Follow up-Plant Operations
Follow up-Maintenance
Prompt Onsite Response to Events at Operating
Power Reactor
Implementation of Generic Letter 89-10
ITEMS OPENED
DISCUSSED
AND CLOSED
OPENED
~T
e
Item Number
IFI
260,296/97-11-01
260.296/97-11-02
260,296/97-11-03
DEV
260,296/97-11-04
260,296/97-11-05
260,296/97-11-06
CLOSED
T~e
Item Number
.260/96-06-02
260/96-05-03
IFI
260,296/95-19-01
Status
Open
Open
Open
Open
Closed
Open
Status
Closed
Closed
Closed
Descri tion and Reference
Status
Control Issues
(Section 01.2)
Failure to Control
CREV Switch
Position (Section 01.3)
Adequacy of CREV Standby Train
Circuit Testing (Section 01.3)
Inadequate
Procedural
Controls for
MOV Activities (Section El.3)
Inadequate
Design Assumptions for
MOV Capability (Section E1.3)
Failure to Prepare the Trend Report
Required
by Procedures
(Section
El. 3)
Descri tion and Reference
Failure to: Perform
Evaluation Prior to Disabling
(Section 08. 1)
Customer
Group Workers
Exceeded
Overtime Limits Without Approved
Exemption (Section 08.2)
Reduced
Scope of Valves in GL 89-10
Program (Section E8.3)
k
'1
~QN
0
0
0