ML18039A233

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Insp Repts 50-259/97-11,50-260/97-11 & 50-296/97-11 on 971026-1206.Violations & Deviations Noted.Major Areas Inspected:Operations,Engineering,Maint & Plant Support
ML18039A233
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 01/02/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18039A230 List:
References
50-259-97-11, 50-260-97-11, 50-296-97-11, NUDOCS 9801210278
Download: ML18039A233 (64)


See also: IR 05000259/1997011

Text

U.S.

NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

License

Nos:

Report

Nos:

Licensee:

Facility:

Location:

Dates:

Inspectors:

50-259,

50-260,

50-296

DPR-33,

DPR-52,

DPR-68

50-259/97-11,

50-260/97-11,

50-296/97-11

Tennessee

Valley Authority

Browns Ferry Nuclear Plant,

Units 1, 2,

8 3

Corner of Shaw and Browns Ferry Roads

Athens,

AL

35611

October

26 - December

6,

1997

L. Wert, Senior Resident 'Inspector

J. Starefos,

Resident

Inspector

E.

Di Paolo.

Resident

Inspector

E. Girard,

Reactor

Inspector

(Section

E1.3)

Accompanying Personnel:

T. Scarbrough,

NRR

R.

Wessman,

NRR

Approved by:

M. Lesser,

Chief

Reactor Projects

Branch

6

Division of Reactor

Projects

980i2i0278 980i02

PDR

ADQCK 05000259

8

PDR

0

EXECUTIVE SUMMARY

Browns Ferry Nuclear Plant, Units 1, 2,

8 3

NRC Inspecti'on Report 50-259/97-11,

50-260/97-11.

50-296/97-11

This integrated

inspection included aspects

of licensee

operati'ons,

engineering,

maintenance,

and plant support.

The report covers

a six-week

period of resident inspection

and

an inspection of the licensee's

motor-

operated

valve

(GL 89-10) program.

~0er ati ons

Operator actions in response

to a Unit 2 single control rod insertion

and

reactor

scram were good.

Procedures

were actively referenced

and correctly

followed.

Good performance

was noted

on the part of the assistant

unit

operator that identified an

EHC fluid leak during performance of rounds.

,(Section 01.1)

Procedural

controls of the control

room emergency ventilation

(CREV) system

priority selector

swi,tch were not adequate

to ensure that the switch was

maintained in the correct position.

(Violation 260,296/97-11-02,

Failure to

Control

CREV Switch Position,

Section 01.3)

Further review is necessary

regarding testing, of the transfer control circuitry.

(Unresolved

Item

260,296/97-11-03,

Adequacy of CREV Standby Train Circuit Testing,

Section

01.3)

Two examples of status

control issues

were identified by the inspectors

during

this inspection.

The first example is addressed

by the violation for

inadequate

control of the

CREV system priority selector switch.

In addition,

the inspectors identified

a drain valve on

a non-safety related service air

compressor that was not .in the requi red position.

Additional

NRC review of

recent status control issues is warranted.

( Inspection Followup Item

260,296/97-11-01,

Status

Control Issues,

Section 01.2).

Adequate

mechanisms

were in place to prompt an annual

licensee

review of

freeze protection equipment.

Small bore and stagnant

piping in

RHRSW pump

rooms could have been given priority during inspection

and repai r of freeze

protection equipment

so that the identified condition of uninsulated

small

bore piping in colder conditions would not have existed.

The licensee'.s

actions to place heaters

in and tarpaul.ins

over the

RHRSW pump rooms provided

a level of protection for the uninsulated piping.

(Section 02.3)

Maintenance

Good mechanical

maintenance

performance

was noted during replacement of the

immersion heater coil assembly

on the 28

EDG.

Effective troubleshooting to

determine the cause of burned lugs in the

EOG control cabinet identified

problems with the immersion heater

even though the heater

appeared to be

working.

(Secti on Ml.1)

ill

il~

~E

Implementation of Generic Letter 89-10 at Browns Ferry was not sufficiently

complete to permit the

NRC to complete its review.

(Section E1.3)

Inspectors identified that the licensee failed to revise procedures

to declare

the applicable

system or train inoperable

when certain motor-operated

valves

'ere

p')aced in their non-safety positions

(Section E1.3)

Inspectors identified that the licensee failed to prepare motor-operated

valve

trend reports in accordance

with procedure

requirements.

(Section E1.3)

The licensee failed to evaluate test data to assess

its:Generic Letter 89-10

program design

assumptions

and improperly used actuator stall efficiency in

evaluating motor-operated

valve operability.

(Section E1.3)

On two occasions

during the inspection period, the

NRC prompted problem

evaluation reports

(PERs) to be written.

The first example

was

an

NRC

identified deficiency with a main steam pressure

instrument calibration

calculation.

The original set point and scaling calculation for the main

steam pressure

instruments

analyzed for a calibration frequency of 12 months

versus the surveillance instruction frequency of 18 months.

(Section

E1. 1)

The second

example involved problems with radiation monitor RH-90-130.

(Section

R2. 1)

In both of these

examples,

personnel

did not initiate PERs

when they were warranted.

Review of the technical operability evaluation

(TOE) to evaluate the main

steam line pressure

transmitters,

which were installed in the plant with

incorrect upper range pressure limits, identified deficiencies with the TOE.

The overall results of the

TOE were not affected.

No regulatory violations

were identified concerning these non-safety related transmitters.

(Section

El. 1)

The licensee properly implemented the Core Operating Limits Report for Unit 2

Cycle

10 with respect to the revised

TS requirements.

(Section

E1.2)

The licensee's

incident investigation

team performed well in investigating the

equipment

issues

which caused

the Unit 2 scram.

The team studied available

information, developed

a theory of the cause,

and in a prompt manner,

performed electrical testing which supported the postulated

cause.

The

investigation into the

EHC fluid leaks

was also thorough

and determined the

cause of the leaks in a reasonable

time period.

(Section

E2. 1)

Although the licensee's

actions to decrease

the oil particulate levels in the

RCIC system were adequate.

the

RCIC oil particulate

level issue represents

another

example of the difficulties that the licensee is experiencing with the

lube oil analysis

program.

(Section E2.2)

ili

Pl ant

Su

ort

Unexpected indications

on the radioactive effluent monitor recorder were not

thoroughly investigated prior to discontinuation of compensatory

actions

required for an inoperable monitor.

The licensee

subsequently

completed

a

detailed

investigation which identified that

a leaking valve had caused the

unexpected

indications.

The investigation 'also concluded that the monitor

was not inoperable

and that regulatory requirements

were met during the

period.

(Section R2.1)

ili

0

Summar

of Plant Status

Re ort Details

Unit 1 remained in a long-term lay-up condition with the reactor defueled.

Unit 2 was brought critical on October

18,

1997. following the cycle 9

refueling outage.

The unit reached full power on October

23.

1997.

Electro-

hydraulic control fluid leaks

on turbine control valves

caused

several

power

decreases

to perform maintenance

during the inspection period.

(Section

E2. 1)

On October 28,

1997. the unit scrammed

when

a

8 reactor protection system

(RPS) relay problem occurred while a half scram

was already present

on the A

RPS system.

(Sections

01. 1,

E2. 1)

The unit was brought critical on October

30,

1997,

and remained at power during the inspection period with the

exception of maintenance

and routine testing

downpowers.

Unit 3 operated

at power with the exception of routine testing

and several

balance of plant maintenance

issues

which required

power decreases.

I. 0 erations

01

Conduct of Operations

01. 1

Unit 2 Sin le Control

Rod Insertion

and Reactor

Scram

a.

Ins ection Sco

e

71707 93702

The resident. inspectors

observed

and reviewed the actions of control

room operators

in response

to two separate

unexpected

plant transients.

In one instance,

a single control rod inserted

unexpectedly

during

repairs of an electrohydraulic

(EHC) fluid leak.

Not directly related

to this incident.

an automatic reactor scram occurred shortly thereafter

due to a problem wi.th reactor protection system relays.

Additional

inspection regarding the cause of the scram is described

in section

E2. 1

of this report.

b.

Observations

and Findin s

At 12:23 p.m.,

on October 28,

1997,

an Assistant Unit Operator, noted

a

decreased

Unit 2

EHC fluid .reservoir level.

It was determined that an

EHC oil leak existed

on the servo mechani.sm for the gl turbine control

valve.

Reactor

power was reduced to allow the valve to be shut for

repai rs.

Upon closing the Pl control valve,

an expected half scram was

received

on

RPS channel

A.

Approximately 2 minutes after receiving the

half scram, control rod 30-23 moved in to the full overtravel position.

One of the resident inspectors

was in the control

room at the time and

observed the rod: insertion.

The inspector

noted that the rod appeared

to travel

from the full out position to the full overtravel position in

less than

5 seconds.

The licensee

commenced corrective actions for the

ili

01.2

2

1

rod drift in accordance with Abnormal Operating Instructi.on,

2-AOI-85-2,

Uncoupled Control

Rod.

This included evaluating thermal limits and

inspecting the

CRD hydraulic control unit (HCU) for abnormalities.

Subsequent

inspection, revealed that the

HCU scram outlet valve f'r

control rod 30-23 was leaking air past its diaphragm.

The licensee

postulated that air pressure

on the scram val.ve was

r educed

by leakage

through this path

and leakage

through 'the "B" powered

scram solenoid

ilot valve (SSPV).

The "A" powered

SSPV was de-energized

due to the

alf scram.

This caused

the scram valve to open

and resulted in the rod

insertion.

At 2:50 p.m., repairs

were completed

on the gl Control Valve (CV).

The

valve was opened

and the half scram

on

RPS channel

A was reset.

At 3:08

PH the operators

reshut the gl CV in order to perform post maintenance

testing.

About

1 minute later, concurrent with the worker releasing

a

button to re-open the

gl CV, the reactor

scrammed.

Operators

completed

scram follow up actions satisfactorily.

Reactor water level decreased

to lowest level of about

-32 inches

and was rapidly restored

by the

feedwater

pumps.

The response of the feedwater

pumps

was

as expected

following the scram.

No safety system problems were observed

associated

with the recovery.

Additional review of,the scram. is described

in

Section

E2.1.

Following the Unit 2 scram,

both SSPVs

and the scram outlet valve

diaphragm,

responsible for the single rod insertion,

were replaced.

One

,of the inspectors

observed satisfactory

scram time testing of the 30-23

control

rod after the work was completed.

Following completion of

corrective actions

(see section

E2. 1),

a reactor

startup

was

commenced

late on October 29,

1997.

Operator performance

and control

room

conduct were observed to be good during the rod withdrawal to

criticality.

Conclusions

The actions oi the control

room operators

in response to these

unexpected

transients

were good.

Procedures

were actively referenced

and correctly followed. The

EHC fluid leak was identified by an

AUO

during the performance of rounds.

Status

Control of 0 erations

E ui ment

Ins ection Sco

e

71707

The inspectors

reviewed the licensee's

corrective actions after

an

incorrectly positioned service air system valve was identified by the

NRC.

Observations

and Findin s

On November 10,

1997.. the inspectors identified that

a drain valve on

the

F service air compressor after-cooler condensate

trap was partially

open

and discharging

a water/air mixture.

This valve had previously

ili

been caution tagged in the throttled open position to remove moisture

buildup since the licensee believed that the trap was not operating

properly.

The caution tag was subsequently

removed

and the valve was

expected to be shut.

The trap is

a float type trap.

The drain valve

drains water from the trap body (vice other designs

which drain from

upstream of the trap).

Operation of the trap bypass will drain water

from the trap body, thus it will take

some time for the body to fill

back up and

commence

automatic trap operation again.

The licensee initiated

a Problem Evaluation Report

(PER) to investigate

the cause of the mispositioned valve.

Operations

management

postulated

that an Assistant Unit Operator

opened the valve to check for moisture

and upon finding a significant quantity of liquid, left it throttled to

complete draining with the intention of returning later to close it.

Although the valve was not in the correct position and did affect the

operation of the trap, overall operation of the service air system

was

not adversely affected.

The

PER evaluation

noted several

other

mispositioned

component incidents since January

1996.

The

PER

corrective actions include

a discussion of the

PER and event with all

shift crews, stressing

the need for open

and honest

communication

concerning errors

and events.

The Operations

Superintendent will

evaluate the use of red valve covers

on valves in the vicinity to act as

a reminder to the operator to re-close the valve.

Operation of this

particular trap with be covered during

AUO requalification training.

Also, the

PER corrective actions indicated that

an engineering

work

request

was issued to address

the adequacy of the condensate

traps

and

the excessive

moisture experienced with the new compressors.

Conclusion

The equipment identified out of the required position was not safety-

related.

The involved equipment

remained operable.

However,

NRC

inspectors identified two examples of status control issues

during the

inspection period.

(See Section 01.3 for the second

example.)

In

recent months, the licensee

has identified other status control issues.

Further review of recent status control issues is warranted.

(Inspection Follow up Item (IFI) 50-260,296/97-11-01,

Status

Control

Issues.)

Control

Room Emer enc

Ventilation S stem Preferred Train Selector

Switch Issues

Ins ection Sco

e

71707

37551

The inspectors

reviewed the effect of having the Control

Room Emergency

Ventilation (CREV) pref'erred selector switch in a position other

than

that required

by work instructions.

Surveillance testing

was reviewed

to determine if the automatic start feature of the

CREV unit was

adequately tested.

ili

0

b.

Obser vati ons

and Findin s

On November

19,

1997,

one of the resident

inspectors identified that the

.CREV system priority selector

switch (0-XSW-031-7214)

was in a position

different than that described in work control instructions.

Work being

performed

on the

CREV system

made the A train inoperable.

Work control

instructions

(planning fragnet) required the preferred unit selector

switch to be placed in the

B position.

The control

room operators

subsequently

placed the switch in the

B position.

The inspector

questioned

the effect of the switch being selected to the .A train which

was inoperable.

Logic diagrams

and control drawings were reviewed.

The inspectors

concluded that the

B train of the

CREV would have operated if called

upon.

This was based

on the standby feature design of the two trains.

Since the A train was selected,

an initiation signal would be sent to

both trains to star t, however, only the preferred train would start

immediately.

The non-preferred

system operation would be delayed for

some time by a timer and flow switch arrangement.

If the proper

flowrate is not sensed

in the preferred

system after

a time delay, the

non-prefer red system would start.

The effect of having the A train

selected

would have resulted in the

8 train starting after

a time delay.

The time delay is incorporated into CREV system design.

Therefore,

the

inspectors

concluded that the switch being in the wrong position did not

effect the operability of the

B train.

The inspectors

also questioned

whether the flow switch/time delay

ci rcuitry was periodically tested.

The flow switch is periodically

calibrated.

However, the time delay relay and associated

contacts

have

not been periodically tested

for both trains.

Review of testing of the

system per surveillance instruction O-SI-4.2.G-2,

Control

Room Isolation

and Pressurization

Functional Test,

indicated that the standby feature,

via the time delay and flow switch arrangement,

when the selector

switch

is selected to the 8 train.

has not been tested

since preoperational

testing of the upgraded

CREV system.

The licensee

determined that the

current Technical Specifications did not specifically requi re testing to

be completed;

however, the Improved Standard

Technical Specifications

(ISTS) that the licensee

has submitted for

NRC approval,

require testing

of the control circuit.

The licensee

developed

a work order to confirm

that the

CREVs train A low flow ci rcuitry would start train A when the

system priority selector switch is in the train

B position.

Testing

will be performed

on the requi red periodicity when

ISTS is implemented.

Additional review of the testing

and potential effects of the standby

train logic failures is necessary.

(Unresolved

Item 50-260,296/97-11-03,

Adequacy of CREV Standby Train Circuit Testing)

The inspectors

concluded that the licensee did not adequately

control

the system priority selector

switch. Operating Instruction 0-0I-31,

Control

Bay and Off-Gas Treatment Building Air Conditioning System,

Revision 49, did not have the appropriate

guidance to maintain the

preferred selector

switch in the correct position.

The procedure did

not address

the switch.

Apparently, the procedure

had not been proper ly

~i

0'

02

02.1

revised

when the

CREV system

was modified in 1993.

The inspector also

observed portions of CREVs testing

on December

1,

1997, during which the

operators

had. to reposition the switch without specific guidance.

This

is identified as Violation 260,296/97-11-02,

Failure to Control

CREV

Switch Position.

Conclusion

Procedural

controls were not adequate'to

ensure that the Control

Room

Emergency Ventilation System priority selector switch was maintained in

the correct position.

Additional review is required to determine if

control circuitry in the

CREV system

was adequately tested.

Operational

Status of Facilities and, Equipment

Auxiliar Unit 0 erator

Rounds/Plant

Tours

Ins ection Sco

e

71707

The inspector

accompanied

the Unit 3 rounds

and control bay auxi,liary

unit operators

(AUO) on plant tours.

The inspection

focused

on AUO

thoroughness

and attentiveness

to overall conditions.

The resident

inspectors

also performed

numerous tours to revi'ew plant conditions.

Observations

and Findin s

The inspector

accompanied

the Unit 3 rounds

AUO on November 25,

1997,

and the control bay

AUO on November

29,

1997.

The operators

were

knowledgeable

about current plant conditions

and equipment status.

The

operators

also demonstrated

knowledge of equipment deficiencies

such

as

water leaks.

oi,l leaks, and out of service equipment.

The Unit 3 rounds

AUO also demonstrated initiative and sensitivity to safety system status

by writing a work request

on

a minor Reactor

Core Isolation Cooling

(RCIC) system oil leak identified during,the tour

.

On November 25,

1997, the inspector

observed

local

manual

speed

adjustment of the 3B recirculation

pump motor generator

(MG) set.

The

speed

adjustment

was performed manually to increase plant power

and

balance recirculation

pump speeds.

due to the recirculation

pump

MG set

clutch scoop tube being locked in position because

the speed controller

was not functioning properly.

The evolution was properly supervised

by

a licensed operator.

The operators

properly referenced

and performed

the procedure.

Good communications

and coordination of the evolution

was observed

between the control

room unit operator

and the personnel

performing the speed

change evolution.

The inspector concluded that the

infrequent evolution was performed in a controlled manner.

The inspectors identified that emergency

equipment cooling water

(EECH)

leakage

from the

3B RHR room cooler

.was not being properly collected.

The licensee corrected the problem.

$g~

0

On December

1,

1997. the inspector noted water leakage

from some of the

Unit 3 drywell sandpit

and vent sleeve drains.

The licensee

postulated

that the source of the water

from the drains

may .be from leakage

past

fuel pool cooling valves to the annulus

between the drywell liner and

concrete structure via an overflowing fuel pool liner leakage drain.

The licensee

experienced

water leaking from several

Unit 3 drywell

penetrations

in February

1997, which may be symptoms of the same

or

a

similar problem.

In addition, during early October

1997, water was

found to be leaking from containment penetrations

for the Unit 3 core

spray

and- the drywell continuous air monitor which could also be

evidence of this problem.

The licensee

documented

the February

1997,

leakage in problem, evaluation

report

(PER) 970400.

,The

PER concluded that the source of the leak

could:not be determined

and that the leak no longer existed.

The

corrective action f'r the

PER was to monitor the penetrations

during the

during the next refueling outage.

The

PER also stated that any further

corrective actions identified by this action item will be added to the

PER by revising the

PER.

The licensee did not document the leakage

identified in October

or December

1997.

Discussions with the licensee

indicated that they were aware of the problem and planned to document

their findings.

Subsequent

to discussions

with the inspectors,

the

li.censee

developed

a troubleshooting

plan to attempt to determine the

cause of the leakage.

The inspectors

also identified that one of the drywell vent sleeve

drains

had no drainage path.

The end of the drain terminates

near the

floor.

Normally the sand pit and vent sleeve drains are cut pipe

ends which would drain to the floor area in the torus

room.

In this

case,

the pipe appeared to penetrate

the floor surface.

The licensee

has initiated

PER 971818 to address

the drainage

path issue.

Conclusion

The local manual

speed

adjustment of the recirculation

pump motor

generator

set

was proper ly supervised

and controlled.

The operators

demonstrated

good communications

and coordination during the evolution.

High sensitivity to safety system status

was demonstrated

by,the

AUOs

demonstrated

by the Unit 3 rounds

AUO by initiating a work request

on

a

minor RCIC turbine oil leak.

Freeze Protection

Ins ection

Ins ection Sco

e

71714 71707

The inspector

reviewed the. working copy of General

Operating Instruction

O-GOI-200-1,

Freeze Protection Inspection.

Additionally, the, Freeze

Protection

Inspection Discrepancy List and portions of electrical

preventive instructions

EPI.-O-OOO-FRZ001.

FRZ002.

FRZ003 were reviewed.

The inspector also performed walkdowns of the

RHRSW pump rooms

and

channel

diesel fire pump area

and reviewed selected

annunciator

response

procedures

for freeze protection equipment fai lures.

hl~

0

Findin s and Observations

Review of the working copy of O-GOI-.200-1,

Freeze Protection Inspection,

indicated that the licensee

had appropriately considered

changes

made to

the in-process

procedure since it was initiated.

The revision to the

procedure

included placing space

heaters

into the

RHRSW pump rooms

and

installing tarpaulins

over the

RHRSW pump rooms.

The inspector questioned

the mechanism which initiated the O-GOI-200-1.

Freeze Protection

Inspection procedure.

The licensee indicated'hat

the

procedure

was initiated when the Operations

Periodic Activity (OPA)

database

launched the freeze protection activity on August

1 of each

year.

The 0-GOI-200-1 procedure

requests

that Electrical Maintenance

initiate the electrical preventive i.nstructions

EPI-0-000-FRZ001.

FRZ002

and,

FRZ003.

Implementation of these

procedures

actually began

when the

repetitive preventive maintenance

task form was implemented

on September

3.

1997.

Discussions with the licensee

indicated plans to have the EPI-

0-000-FRZ001,

FRZ002,

FRZ003 procedures

completed

by December

19,

1997.

The inspector concluded that adequate

mechanisms

were in place to prompt

an annual

licensee

review of freeze protection equipment.

The inspector toured the

RHRSW pump rooms

and the channel

diesel fire

,pump area.

Several

areas

were noted in the

RHRSW pump rooms where small

diameter pressure

instrumentation lines had insulation

removed for

apparent

work associated

with the heat tracing.

There were also

examples of larger diameter piping and flange areas

which were not

insulated.

The licensee

had work requests

listed on the freeze

protection inspection discrepancy list which documented

insulation

missing and/or

damaged in each of the four

RHRSW pump rooms.

The

inspector

considered that since the licensee's

freeze protection

inspection

procedures

were implemented in September,

consideration

could

have been given to identifying and correcting problems with small bore

and stagnant

piping as

a priority so that the current configuration of

uninsulated

small bore piping in colder conditions would not have

existed.

The inspector

noted that the licensee's

actions to place

heaters

in and tarpaulins over'the

RHRSW pump rooms provided

a level of

protection for the uninsulated piping.

During the tour of the channel

diesel fire pump, the inspector

noted

that the engine exhaust

pipe was not insulated in accordance

with

drawing 37W215-2,

note 9, which requi red the calcium silicate insulation

to extend through the roof and terminate at the outlet end of the

exhaust pipe.

The drawing note further stated that the insulation

located outside shall

have

an aluminum jacket.

The actual configuration

terminated the insulation on,.the outside of the roof with,an aluminum

jacket,

but the remainder

of the outside pipe run to the outlet end was

not insulated.

The licensee initiated

a

PER to address

the discrepancy.

The licensee's initial review could not determine

a need for the

insulation.

During the inspection period, the inspector

reviewed the Freeze

Protection

Inspection Discrepancy List as maintained

on the Unit 1

ig~

il~

ik

08

08.1

computer.

The inspector noted earlier in the inspection period that

although the

3C emergency diesel

generator

(EDG) room heater

had

a work

request

card written indicating that the room heater would not come on,

the discrepancy

was not identified on the Freeze Protection

Inspection

Discrepancy List.

In addition, the inspector noted the Freeze

Protection Discrepancy List did not indicate if the discrepancy

was

safety related

as suggested

by the procedural

guidelines.

A subsequent

review of the Freeze Protection Discrepancy List noted that the l,icensee

had enhanced

the list to address

whether

the system is safety related or

not.

The

3C

EDG heater

discrepancy

had been

added to the list.

The inspector

compared the

RHR Service Water System Index,

O-SIMI-23A,

f'r 80 instruments

which were listed as Electrical Maintenance

responsible for periodic maintenance

against the electrical preventive

instruction EPI-O-OOO-FRZ001,

Freeze Protection

Program for

RHRSW Pump

Rooms etc.,

Revision 8, to verify that the instruments

were tested.

No

problems were identified.

During the review of freeze protection program electrical preventive

instructions,

documentation errors were identified associated

with

jumper placement/removal

and lead lifts.

No equipment configuration

issues

were identified.

Conclusion

. Adequate

mechanisms

were in place to prompt an annual

licensee

review of

freeze protection equipment.

Small bore and stagnant piping in RHRSW

pump

rooms could have been given priority during inspection

and repair

of freeze protection equipment

so that the identified condition of

uninsulated

small bore piping in colder conditions would not have

existed.

The licensee's

actions to place heaters

in and tarpaulins

over

the

RHRSW pump rooms provided

a level of protection for the uninsulated

piping.

Miscellaneous

Operations

Issues

(92901)

Closed

Violation 260/96-06-02

Failure to Perform

a 10CFR50.59

Evaluation Prior to Disablin

Annunciator

.

The inspector

verified that

the revisions to Operating Instruction, OI-55, Annunciator

System,

as

described in the response to the violation dated

September

13,

1996 were

completed.

One of'hose actions

was the completion of safety

assessments

for the annunciators

referenced

in the

UFSAR.

The inspector

noted that the reactor vessel

head leakoff annunciator

had been disabled

on October 31,

1997.

With the assistance

of Operations

personnel,

the

inspector obtained

a copy of the safety assessment

performed for this

annunciator.

The assessment

had been completed

on July 31,

1996.

The

inspector

verified that the assessment

adequately

addressed

the aspects

of the annunciator

referenced

in the

UFSAR.

The inspector verified that

the requirements

in OI-55 had been

met for disabling the annunciator.

The inspector

noted that this was not the first cycle in which the alarm

was .disabled

and reviewed the licensee's

actions to resolve the issue

causing the problem.

After review of work orders,

examination of the

il~

il

pressure

gage indications,

and discussion with engineering

personnel,

the inspector

concluded that the licensee's

actions to resolve the issue

have been progressive

and reasonable.

The determination that the inner

seal

ring is leaking seems

accurate.

Operation with just the outer seal

ring is described

in the

UFSAR.

The licensee

has also listed resolution

of the leaking seal

on the Plant Equipment Action List and is continuing

to pursue resolution.

The violation is closed.

Closed

Violation 260/96-05-03

Customer

Grou

Workers

Exceeded

Overtime Limits Without A

roved

Exem tion.

This violation was

originally discussed

in IR 96-05.

The licensee's

corrective actions

were reviewed.

The inspector

performed

a sample audit of Customer

Group

personnel

work hours during the recent Unit 2 refueling outage.

The

review showed that the proper approvals

were made for overtime hours

which deviated'rom the licensee's

overtime restriction procedure.

The

inspector

also notes that management

stressed,

at plan of the day

meetings during the outage.

the importance for proper approvals for

overtime deviations.

The inspector

concluded that the licensee's

corrective actions were adequate.

The violation is closed.

Conduct of Maintenance

II. Maintenance

Mechanical

Maintenance

Observation

Ins ection Sco

e

62707

The inspector

observed

mechanical

maintenance

work to replace the Unit 1

and

2

B emergency diesel

generator

(EDG) cooling water immersion heater.

Observations

and Findin s

On December

1,

1997, the inspector

observed

mechanical

maintenance

work

to replace the cooling water immersion heater in the Unit 1 and

2

B

emergency diesel

generator.

Discussion with the licensee

indicated that

during troubleshooting to determine the cause of burned lugs in the

EDG

control cabinet, testing indicated that problems

may be present with the

immersion heater

even though the heater

appeared to be working.

Mechanical

maintenance

drained the

EDG cooling 'water system

and replaced

the immersion heater coil assembly.

The maintenance

craftsmen

replaced

the coil assembly in accordance

with the step text in work order

(WO)

97-011442-001.

The inspector

noted that the craftsmen

stopped to have

the

WO step text revised when, necessary.

The immersion heater coil

assembly that was

removed

from. the

EDG was found in a degraded

condition.

The decision to replace the immersion heater

coil assembly

was appropriate.

E

il~

il~

il

Conclusions

10

Good mechanical

maintenance

performance

was noted during replacement of

the immersion heater coil assembly

on the

2B EDG.

Effective

troubleshooting to determine the cause of burned lugs in the

EDG control

cabinet identified problems with the immersion heater

even though the

heater

appeared to be working.

Conduct of Engineering

III. En ineerin

Incorrect Hain Steam Pressure

Detectors

Installed in Plant

Ins ection Sco

e

37551

The inspector evaluated

the licensee's

technical operability evaluation

(TOE) performed to evaluate

main steam pressure

detectors with different

upper range limits than specified in the set point and scaling

calculation document.

The inspector also reviewed the licensee's

corrective actions for

an inspector

identified incorrect calibration

frequency calculation for some of the pressure

instruments.

Observations

and Findin s

The inspector

reviewed licensee corrective actions for pressure

detectors installed in the main steam

system which had different upper

range limits than specified in the licensee's

set point and scaling

calculation documents.

A maintenance

worker replacing

a failed pressure

detector identified the condition.

The installed transmitters

were

Rosemount

Hodel

1153GB wi,th a range

code

9 (0-3000 psig) vice the

specified

range

code

8 (0-1000 psig).

One group of the pressure transmitters

detect

main steam pressure

and

input into primary containment isolation system logic to initiate

closure of the main steam isolation valves

on low steam line pressure.

The other group of pressure transmitters

detect turbine first stage

pressure

and input into the reactor protection system to provide

a

signal to bypass the scram protective feature

on turbine stop

or control

valve closure at power levels less than

30K (corresponding with a first

stage

pressure of 154 psig).

The instruments

are not safety related,

however the setpoints

are controlled by TS.

As part of the original design.

selected transmitters

were to be changed

from range

code

9 (0-3000 psig) to range

code

8 (0-1000 psig) using

a

conversion kit.

Subsequently,

a Part

21 notice for this model

transmitter requi red their return to the vendor for maintenance

during

is

11

Unit 2 recovery.

Non-converted transmitters

were sent to the vendor.

Subsequently,

the range

code

9 transmitters

were installed in Unit 2.

A

walkdown of Unit 3 showed that the proper transmitters

were installed.

No violation of regulatory requi rements

occurred since the transmitters

were not safety related.

The licensee

performed

a Technical Operabi.lity Evaluation

(TOE) since

errors

caused

by drift, instrument accuracy,

and ambient temperature

are

dependent

on the upper

range limit of the instrument.

The

TOE

determined that the instruments

were operable.

The inspector

reviewed the site standard

procedure

(SSP)

SSP-12.57.

Engineering Evaluations for Operability Determination,

the Final Safety

Analysis Report

(FSAR), set point and scaling documents,

calculations,

and the applicable vendor manual.

The inspector

found that the

TOE

technically supported

operabi li.ty of the instruments.

The inspector

noted the following deficiencies:

~

The temperature

band

used to calculate the ambient temperature

errors

was different than used in the original calculation.

No

justification for the

new band was provided.

~

Set point and scaling

document information about environmental

ualification and class

(safety related or quality related)

were

ifferent than that specified in the master

equipment list.

~

The original set point and scaling calculation for the main steam

pressure

instruments

analyzed for a calibration frequency of 12

months vice the surveillance instruction requirement of 18 months.

The licensee

subsequently

revised the TOE. the set point and scaling

document,

and the main steam pressure

instrument calculation

based

on

the inspector's

findings.

The discrepancies

did not affect the overall

results of the

TOE or the acceptability of an

18 month calibration

frequency for the main steam pressure

instruments.

A separate

PER was not initially generated

concerning the incorrect main

steam pressure

instrument calibration calculation although the situation

warranted

one.

The inspectors

brought this issue to licensee

management

attention.

Subsequently.

a separate

PER was generated.

c.

Conclusion

Although the technical operability evaluation

was technically

acceptable,

the inspector identified several

deficiencies in the

documented

evaluation.

The individuals involved were reluctant to

generate

a separate

PER concerning

.the incorrect calibration frequency

calculation.

The maintenance

worker who identified the incorrect

installed instruments

demonstrated

a good questioning attitude.

0

0

0

1

Core 0 eratin

Limits Re ort

12

Ins ection Sco

e

37551

The inspector

reviewed the Core Operating Limits, Report for the Unit 2

Cycle 10 operation for compliance with TS.

Observations

and Findin s

Recent

changes to Uni.t 2 TS were made to incorporate the Unit 2 outage

upgrade of the power range neutron monitor instrumentation.

Changes to

thermal limits specifications

were also

made to implement average

power

range monitor and rod block monitor

TS improvements,

and

maximum

extended

load line limit analyses.

The inspector

reviewed the core

operating limits report to ensure

compliance with the revised

TS

requi rements..

No problems were noted.

Conclusions

The inspector

concluded that the licensee properly implemented the Core

Operating Limits Report f'r Unit 2 Cycle

10 in accordance

with the

revised

TS requirements.

Im lementation of Generic Letter

GL 89-10 "Safet -Related Motor-

0 crated

Valve Testin

and Surveillance"

Ins ection

Sco

e

Tem orar

Instruction 2515/109

This inspection provided

an assessment

of the licensee's

implementation

of GL 89-10.

The licensee notified the

NRC that they had completed

implementation of GL 89-10 in letters dated January

9.

1995, for Unit 2

and January

30,

1996 for Unit 3.

In July 1995 the

NRC conducted

an inspection of the

GL 89-10 program and

documented

the results of that inspection in Inspection Report 50-259,

260, 296/95-19.

The inspectors

concluded that the licensee

had

implemented

GL 89-10 for Unit 2 in a satisfactory

manner.

The

inspectors

found that the assumed

values for valve factor,

stem friction

coefficient,

and rate of loading, which the licensee

had used in

determining the settings

and capabilities

for GL 89-10 motor-operated

valves

(HOVs), were .principally based'n

data

from TVA nuclear

power

plants.

The licensee

indicated that it planned to update the data

supporting the assumed

values

and to make adjustments

to the

HOV

settings.

when and where appropriate.

to ensure that the

HOVs were set-

up using correct data.

Additional

HOV testing

and evaluations

were to

be performed to complete implementation of GL 89-10 for Unit 3.

The

licensee's

removal of a number of motor-operated

valves from the scope

of the

GL 89-10 program was observed

and questioned

during the

inspection

and was identified as

an inspector follow up item.

In September

1995 the

NRC conducted

a further inspection of the

GL 89-10

program at Browns Ferry, concentrating

on Unit 3.

As documented

in

0

Cl

13

Inspection Report 50-259,

260, 296/95-53,

the inspectors

concluded that

the licensee's

implementation of GL 89-10 for Unit 3 was in the process

of being satisfactorily compl'eted.

The inspectors

were unable to make

a

final assessment.

The licensee

had not completed the testing

and

evaluation of the Unit 3 GL 89-10 program

MOVs.

No Unit 3

HOV test data

were available for inspector

review.

The inspector follow up item

concerning the licensee's

reduction of the

GL 89-10'rogram

scope

remained

open.

The current inspection

was conducted to verify that the licensee

had

satisfactorily completed

implementation of GL 89-10 for both Units 2 and

3.

The principal areas

examined were the previously identified

inspector follow up item regarding

program scope,

the final

HOV switch

setting determinations

and verifications of HOV capabilities established

from the completed testing.

and trending of HOV test

and history data.

The inspection also included

a review of the periodic verification

.

requirements

specified

by the licensee's

GL 89-10 program,

a record

review to verify removal of HOV motor brakes,

and

a plant walkdown to

observe the general

condition of MOVs.

The inspection

was conducted

through

a review of the licensee's

GL 89-10

implementing documentation,

interviews with licensee

personnel,

and

observation of MOVs in the plant.

The documents

reviewed included:

o

'VA Nuclear Standard

Department

Procedure

MMDP-5,

"HOV Program,"

Revision 1, dated

September

26,

1997.

o

TVA Standard

Engineering

Procedure

DS-M18.2.21,

"Motor Operated

Valve Thrust and Torque Calculation," Revision 8, dated July 15,

1996.

~

TVA Mechanical

Design Standard

DS-M18.2.22,

"MOV Design Basis

Review Methodology.

Revision

1. dated July 29,

1991.

~

Calculation MD-Q0999-910034,

"NRC Generic Letter 89-10 - Motor

Operated

Valve Evaluation," Revision

13.

o

Other documents

referred to in the following paragraphs.

o

Summary tabulations of MOV information and calculation results

prepared

by the licensee.

Prominent

among the tabulations

referred to above

was

a list of

"available valve,factors"

(AVFs) for the licensee's

GL 89-10 gate

and

globe valves.

The AVFs were calculated

using formulas described in

revious inspection reports

(e.g.,

Inspection Report 50-338,

339/97-01).

he inspectors

compared the AVFs for the licensee's

GL 89-10

HOVs to

valve factor requirements

established

in industry testing which the

NRC

had previously reviewed.

These

comparisons

were performed to determine

if the licensee's

AVFs were reasonable.

0

0

4l

b.

Observations

and Findin s

14

1.

Sco

e of MOVs Included in the

GL 89-10 Pro ram

A reduction in the scope of MOVs included in the Browns Ferry GL 89-10

rogram was questioned

during Inspection 50-260,

296/95-19.

The

icensee

had reduced the scopes for Units 2 and

3 from 56

MOVs each to

36 MOVs each,

based

on a re-evaluation -of the functions of the

MOVs.

This reduction in scope

was identified for further review as Inspector

Follow up Item (IFI) 50-260(296)/95019-01,

Reduced

Scope of Valves in GL 89-10 Program.

In a letter dated

October

7,

1996. the

NRC informed the licensee that it

had concluded that the criteria used

by TVA in re-evaluating

the safety

functions of the Browns Ferry

MOVs were unsatisfactory

and

may have

resulted in inappropriate

removal of MOVs from the Browns Ferry GL 89-10

rogram.

An assessment

for the valves

removed

was enclosed with the

etter.

The

NRC requested

the licensee to re-examine the safety

functions of the Browns Ferry

HOVs consistent with the

NRC assessment

and to provide any appropriate corrections

to the

GL 89-10 program.

The

licensee

was asked to notify the

NRC of the findings of the re-

examination

and the actions taken

as

a result of those findings.

In a letter dated January

6,

1997. the licensee

provided

a response to

the NRC's request for re-evaluation of the safety functions of the

MOVs

removed from, or not included in, the Browns Ferry GL 89-10 program.

The licensee

stated that

15

MOVs were being added to the individual

GL 89-10 sub-programs

for Units 2 and 3.

The licensee

also stated that

plant procedures

were being revised to require that the applicable

system,

or train, for 18

MOVs (per unit) be declared

inoperable if the

valve was taken out of its normal (i.e.. safety) position for testing.

The licensee

noted that the applicable

Browns Ferry Technical

Specification Limiting Conditions for Operation would govern until such

testing

was completed

and the valve was returned to its normal position.

The letter identified the involved

MOVs and the dates

when these

commitment actions would be implemented.

The addition of 15 valves to

each unit's sub-program

was to be completed

by January

31,

1997.

The

procedure

changes

regarding operability during testing f'r 18

MOVs were

to be completed

by February

21,

1997.

During this inspection,

the inspectors verified that the 15

MOVs listed

in the licensee's

letter of January

6.

1997,

had been included in the

GL 89-10 sub-programs

for Browns Ferry Units 2 and 3.

The GL 89-10 sub-

programs for Units 2 and 3 at Browns Ferry each contained

34 gate valves

and

17 globe valves.

The inspectors

reviewed

a sample of the related

licensee's

procedures

to determine whether the associated

system or

train would be declared

inoperable

when any of the identified 18 MOVs

were placed in their non-safety positions.

The inspectors

found that

the licensee fai'led to provide the appropriate

procedural

requi rements

for several

MOVs.

For example,

Surveillance Instruction (SI) 3-SI-

4.5.B. l.c(II), Revision 9, did not declare Unit 3

RHR Loop II inoperable

when

MOV 3-FCV-74-66 was cycled.

Similarly, SI 2-SI-4.5.B.l.c(II),

Revision 21, did not declare Unit 2

RHR Loop II inoperable

when

MOV 2-

FCV-74-66 was cycled.

The licensee's

failure to revise plant procedures

in accordance

with its January

6,

1997 letter is

a deviation from a

commitment (260,296/97-11-04).

2.

Determinations of Settin

s and Verifications of MOV Ca abilities

'I

Switch Settin

s

The licensee controlled the operation of MOVs in its GL 89-10 program

.

through

a combination of torque

and limit switches.

The torque switch

was bypassed

in the closing di rection for 95 to 98K of stroke length as

confirmed

by diagnostic data.

For opening,

the torque switch was

bypassed

for the entire stroke.

The licensee calculated the thrust and torque requirements

for MOVs in

the

GL 89-10 program using standard

industry equations.

The predicted

thrust requirements

for gate valves were calculated typically assuming

a

.0.4 valve factor with a 20K safety factor .

For globe valves,

the

licensee

assumed

a valve factor of 1.0 for closing and 1.2 for opening.

The licensee typically assumed

a stem friction coefficient of 0. 15 and

margin for potential

reduction in thrust output under

dynamic conditions

(referred to as rate of loading) of 10K for gate valves

and

15K for

globe valves.

'For MOVs with roller-screw stem nuts, the licensee

based

the stem friction .coefficient on manufacturer's

information.

Oiagnostic

error and torque switch repeatabi lity were accounted

for in the switch

setting cal'culations.

The licensee established its assumptions

for

determining predicted thrust

and torque requirements

based

on test data

principally from Browns Ferry and other

TVA nuclear

power plants.

The inspectors

noted that thrust settings for a few MOVs at Browns Ferry

had .not been

updated in the controlling setting drawings to reflect the

results of the dynamic tests

performed earlier in 1997.

The licensee

acknowledged that its

MOV setting drawings

needed to be updated.

Accuracy of the

MOV setting drawings will be re-evaluated prior to the

NRC closing its review of the Browns Ferry GL 89-10 program.

For some

MOVs, the licensee

assumed

run efficiency in the closing

direction when predicting the torque output capability of its actuators.

The inspectors

noted. that the actuator manufacturer

is preparing

new

guidelines that might affect the acceptability of the licensee's

use of

run efficiency.

Licensee

personnel

stated that they were aware of this

situation

and would address

the capability of the affected

MOVs when the

new guidance

was issued.

Oesi n-Basis

Ca abilit

At Browns Ferry, the licensee

had dynamically tested

8 gate valves

and

7

globe valves in Unit 2,

and

5 gate valves

and

7 globe valves in Unit 3

16

as part of its GL 89-10 program.

The test data for each of these valves

was used to establish its valve factor,

stem friction coefficient,

and

rate of'oading.

Using these,

the calculations

and settings

for. each of

the dynamically tested

valves were revised.

For

MOVs tested at partial design-basis

differential pressure

conditions,

the licensee extrapolated test data

from test conditions to

design-basis

conditions in evaluating thrust

and torque requi rements.

Appendix

E of MMDP-5 provided guidelines for in-plant differential

pressure testing of MOVs at Browns Ferry.

The inspectors

noted, that the

guidelines did not clear ly address test conditions that would provide

sufficient contact load to assure reliable data.

The inspectors

did not

identify any cases

where this resulted in unsatisfactory

data.

The

licensee

agreed that clarification was appropriate

and indicated that

additional

guidance for test setup conditions,

such

as prepared

by the

Electric Power

Research

Institute, would be provided to ensure reliable

extrapolation of dynamic test data.

For the non-dynamically tested

valves,

Browns Ferry still relied on the

general

valve factor assumptions

(e.g..

0.4 for gate valves) established

by the licensee's

corporate office for determining the predicted thrust

and torque requi rements.

It had not formally assessed

the validity of

these

assumptions

based

on test information.

The inspectors

found that

some of the results

from tests

performed at Browns Ferry did not support

the assumptions.

For example.

dynamic tests

completed at Browns Ferry

in 1995 (subsequent

to previous

NRC GL 89-10 inspections)

on

MOVs 3-FCV-

75-09,

3-FCV-75-37,

and 3-FCV-74-71 revealed

gate valve factors of 0.6

or greater.

The inspectors

also noted that the licensee

had not

performed

a documented

evaluation of the test data to verify the

adequacy of the program assumptions

for stem friction coefficient and

rate of loading effects.

The licensee's

fai lure to evaluate

dynamic

test data in relationship to its

GL 89-10 program assumptions

could have

resulted in MOVs being incapable of performing their safety functions.

The inspectors

found that the issue of the licensee's

failure to assess

the validity of its assumptions,

as discussed

in the preceding

paragraph,

had been identified in a licensee

self-assessment

conducted

in May 1997.

In the self-assessment

report dated

November 7,

1997, the

licensee

determined that the Browns 'Ferry GL 89-10 program was not

adequate

to support

an

NRC inspection of GL 89-10 implementation.

One

of the recommendations

in the self-assessment

report was that

justifications and analyses

were needed to strengthen

the basis for the

assumed

valve factor and other appropriate factors.

This was identified

for. resolution in Browns Ferry Problem Evaluation Report

(PER)

971770

(initiated on November

12,

1997).

The

PER stated that the licensee's

corporate

engineering office had issued

a white paper that concluded

that

a valve friction factor of 0.6 should

be used for gate valves that

could not be dynamically tested.

The

PER also indicated that the valve

factor guidance provided in Design Standard

DS-M18.2.21

was inadequate

and that .an evaluation of the

MOVs in the

GL 89-10 program was required

to ensure the abi'lity of these

MOVs to perform their safety functions.

Using

a valve factor of 0.6 for gate 'valves

and 1.2 for globe valves,

'

0

17

the licensee

reviewed the capability of its GL 89-10

MOVs to perform

.their safety functions.

In some cases,

the licensee relied on actual

dynamic test data

or bypass of the torque switch to justify the

operability of'ts

MOVs.

The licensee

was currently completing its

plans for justifying the design assumptions

for valve factor,

stem

friction coefficient and rate of loading effects.

In a letter dated

December

15,

1997. the licensee indicated it would revise its GL 89-10

program by January

30,

1998, to address

issues

such

as the adequacy of

the design assumptions.

The inspectors

considered

the licensee's

failure to evaluate test data to assess

its GL 89-10 program design

assumptions

to be

a violation of the requi rements of 10 CFR 50 'ppendix

B, Criterion III, "Design Control."

The inspectors verified that the

violation was not repetitive.

This non-repetitive,

licensee-identified

and corrected violation is being treated

as

a Non-Cited Violation,

consistent with Section VII.B.1 of the

NRC Enforcement Policy (50-

260,296/97-11-05).

Another example is identified in a subsequent

paragraph of this report section.

The inspectors

found that the licensee

had incorrectly evaluated

the

operability of'everal

MOVs in Problem Evaluation Report

(PER)

940066

(initiated on March 22,

1994).

In the evaluation,

the licensee

had

relied on the "stall efficiency" of MOV actuators to evaluate the

operability of the

MOVs.

The actuator

manufacturer

had provided

a value

for stall efficiency for'se by licensees

in evaluating potential

structural

damage in the event of an actuator

motor stall condition.

The manufacturer,

Limitorque, specifically stated that the use of stall

efficiency .was not reliable for predicting actuator output capability.

For example,

see Limitorque Haintenance

Update 92-1 (issued in 1992) or

Application Guide for Motor-Operated

Valves in Nuclear

Power Plants,

(NP-

6660-D, dated

March 1990) prepared

by the Electric Power

Research

Institute.

A current evaluation using the appropriate efficiency showed

that the valves

had been operable..

However, the inappropriate

use of

stall efficiency in predicting actuator output could have resulted in

the licensee

not recognizing

an inoperable condition of a safety-related

MOV.

The inspectors

considered

the licensee's

use of stall efficiency

to represent

a violation of the requirements

of Criterion III of 10 CFR 50, Appendix B, Design Control.

The inspectors

found that the licensee

had recognized that use of stall efficiency .was inappropriate

and that

evaluations

subsequent

to

PER 940066 did not use stall efficiency.

For

example,

the licensee

evaluated the operability of its GL 89-10

MOVs in

its recent

PER 971770 using pullout or run efficiency (rather

than stall

efficiency) together with consideration of the applicable motor curves.

The inspectors verified that the"violation was not repetitive.

This

non-repetitive,

licensee-identified

and corrected violation is being

treated

as

a Non-Cited Violation, consistent with Section VII.B.1 of the

NRC Enforcement Policy (50-260,296/97-11-05).

Another example is

identified in a preceding

paragraph of this report section.

0

0

0

MOV De radation

18

The inspectors

found that the licensee

had not provided clear guidance

for addressing

potential degradation of HOV performance.

The licensee

agreed that its guidance could be clarified and initiated steps

for this

action.

3

M~QV T

di

GL 89-10 suggested

that

MOV data

on failures

and corrective actions

(including repairs,

analyses,

as-found deteriorated

conditions, etc.)

be

periodically examined at least every two years or after each refueling

outage to establish

trends in MOV operability.

Currently, the licensee

implemented this trending through requi rements in Procedure

MHDP-5.

Until'evision 0 of MMDP-5, became effective on August 20.

1997, the

trending requirements

were specified

by Site Standard

Practice

SSP-6.51,

"Program Plan for Generic Letter 89-10," Revision 3

~ effective January

10,

1996.

MMDP-5 requi red issuance of an

MOV trending report at the

completion of every testing cycle (18 months or end of each refueling

outage).

The report was to include (1)

MOV signature analysis report

and (2) maintenance

history (corrective

and preventive).

SSP-6.51

had

required

a similar report at the same periodicity.

The inspectors

found

that the licensee

had not prepared the trending report required

by the

rocedures.

The licensee's

failure to prepare the trend report required

y procedures

is

a violation of 10 CFR. 50. Appendix B, Criterion V,

"Procedures"

(50-260,296/97-11-06).

4.

Periodic Verification of MOV Ca abilit

In Section 3. 13 of MMDP-5, the licensee stated that the purpose of

periodic monitoring of MOVs was to ensure

continued

MOV ability to

function under

design-basis

conditions,

and to identify isolated or

generic problems with MOVs or the overall program.

MNDP-5 also noted

that periodic verification should identify deterioration of MOV

components

before significant degradation

occurs.

MMDP-5 indicated that

the licensee

was working with the owners groups to share test data.

In

a letter to the

NRC dated

March 17,

1997, the licensee stated that it

was participating in a joint owners group program in response to GL 96-

05, Periodic Verification of Design-Basis Capability of Safety-Related

Motor-Operated

Valves.

The licensee's

plans for MOV periodic

verification were found to be adequate for GL 89-10.

The

NRC may re-

assess

the licensee's

long-term

MOV periodic verification program as

part of its review for GL 96-05.

I

5.

Walkdown

The inspectors

conducted

.a plant walkdown of MOVs to- assess

their

condition.

A previous walkdown described

in Inspection Report 50-259,

260, 296/95-53,

reported that cover bolts were loose or missing

on

several

MOVs.

The inspectors

did not observe

any similar examples

during the current inspection.

The inspectors

noted

a significant

difference in the quality of stem grease

applied to various

MOVs. This

0

1

0

19

was apparently

due to the licensee's

past

use of different stem greases.

A future closeout inspection for GL 89-10 will examine whether the

licensee's justification of'tem friction coefficient and rate of

loading effects are applicable to the different greases

or a possible

mixture of the greases.

The inspectors

al'so observed the presence of a

plastic cap

on an actuator

grease relief line for one

HOV (2-FCV-74-

106).

This was not

a

GL 89-10

HOV.

The licensee

acknowledged

the

inspectors'alkdown

findings and stated that appropriate action would

be taken.

6.

Motor Brakes

Inspection

Report 50-259,

260, 296/95-53 indicated that motor brakes

had

not been

removed from HOVs 3-FCV-73-34, 40,

and 44.

During the current

inspection,

the inspectors

reviewed documentation

attached to BFPER

940038 which verified that the brakes

had been

removed.

c.

Conclusions

Implementation of GL 89-10 at Browns Ferry was not sufficiently

developed to permit the

NRC to complete its review.

The inspectors

did

not identify any immediate operability concerns with GL 89-10 .HOVs at

Browns Ferry.

The inspectors

identif'ied a violation involving the licensee's

failure

repare

a trend report required

by procedures

and

a deviation from a

icensee

commitment to revise procedures

to assure

the applicable

system

or train for certain

HOVs would be declared

inoperable

when the

MOVs

were placed in thei r non-safety positions during operation.

In

addition,

a non-cited violation resulted

from (1)

a failure to evaluate

HOV test data to verify that it supported

GL 89-10 program design

assumptions

and (2) improper use of actuator stall efficiency.

A summary of the principal actions to be performed

by the licensee to

address

the issues identified in this inspection

and complete

implementation of GL 89-10 is as follows:

Preparation of test-based

justifications for the valve factor,

stem friction coefficient,

and rate of loading assumed

in the

design calculations for each

GL 89-10

HOV (including MOVs with

special

features

such

as roller screw stem nuts, different stem

greases.

or mixed stem greases).

(Refer to NCV 50-260,296/97-11-

05)

Updating of calculations

and

HOV setting drawings

based

on the

justified assumptions.

Implementation of trend reporting based

on the periodic reviews

recommended

by GL 89-10.

(Refer to VIO 50-260,

296/97-11-06)

E2

E2.1

20

~

Correction of procedures

that did not implement the licensee's

commitment to assure that the applicable

system or train for

certain

HOVs would be declared

inoperable

when the

HOVs were

placed in their non-safety positions during operation.

(Refer to

DEV 50-260.296/97-11-04)

In a letter

dated

December

15.

1997, the licensee

committed to revise

the Browns Ferry GL 89-10 program by January

30,

1998, to address

the

design input issues identified during this inspection.

Further, the

licensee

committed to revise its

MOV design ca1culations to reflect the

GL 89-10 program design input revisions

by Harch 31,

1998, for Unit 3,

and August 31.

1998, for Unit 2.

The

NRC will re-inspect the

GL 89-10

program at Browns Ferry following notification from the licensee that

the issues

described in this report are sufficiently resolved to permit

verification that the intent of GL 89-10 has

been met.

The licensee

stated that

a status letter would be provided to the

NRC by March 2.

1998, indicating its progress

in completing the commitment actions.

Engineering

Support of Facilities and Equipment

Unit 2 Reactor

Scram

Due to

EHC Leak and Reactor

Protection

S stem Rela

Problem

Ins ection Sco

e

37551

93702

The inspectors

monitored

and reviewed the licensee's

investigation

and

corrective actions following a Unit 2,reactor

scram.

Observations

and Findin s

After the Unit 2 reactor

scram

on October 28,

1997, the licensee

appointed

an Incident Investigation (II) team headed

by an engineering

manager to determine the cause of the scram.

Some initial information

indicated that

a scram air header

pressure

problem was involved.

Later

on October

28, the licensee

simulated the same conditions which existed

when the scram was received

and inspected

the air system.

No problems

were found.

The low pressure

was subsequently

determined to have

occurred after the scram

as expected.

The inspectors

reviewed

information relating to previous

scrams

which supported the conclusion

that the scram air system

had performed

as expected.

The investigation continued

and early on October 29. the II team

developed

a postulated

cause of the scram.

Additional troubleshooting

and, diagnostic testing enabled the team to conclude the following

sequence

of events

associated

with the scram:

A half scram was present

on the A side of the Reactor

Protection

System

(RPS)

due to the g1 turbine control valve (CV) being closed

for repair of an electrohydraulic control fluid leak.

The 5A-K14B relay, associated

with the Bl RPS ci rcuitry,

unexpectedly

de-energized.

The team found this through

a detailed

0

0

21

review of computer information involving relay conditions at the

time of the scram.

The 5A-K14B relay has contacts

in the

RPS

circuitry which serve to de-energize

some of the scram solenoid

ilot valves

(as well as other functions). It is located at the

ottom of a long sequence of normally shut contacts,

any of which

open to initiate

a scram signal.

Two of those contacts

are from

one

GE HFA relay connected to the

CV fast closure circuitry which

senses

CV closure

as

a function of EHC pressure

at the valve.

The

parallel relay (5A-K14F) in the Bl RPS circuitry did not de-

energize.

The licensee

performed testing which showed that,

on

decreasing

voltage, the 5A-K14B relay contacts

began to chatter or

cycle at

a voltage value above that at which the relay (and the

5A-K14F relay) de-energized.

The 5A-K14B relay which is

a

CR105

contactor,

was replaced

and tested.

The relay will be examined

for more information on the failure mechanism.

The other

RPS scram.

solenoid pilot valve relays were also tested

and no others

were

found to display the characteristics

seen

on the 5A-K14B.

The licensee

also conducted cycling of the turbine control valves

and monitored pressure

indications at the point that

a turbine

control valve fast closure signal

(decreasing

EHC pressure)

would

be sensed.

The testing

showed that cycling of the valves

caused

notable

(300-400 psig)

downward spikes in

EHC fluid pressure.

Subsequently,

the licensee

indicated that modification of the

EHC

'ystem to reduce these osci llations (installation of orifices) was

being considered.

~

Despite testing,

the licensee

did not find any problem with the

turbine fast closure relay which has two contacts in the Bl RPS

circuitry to the 5A-K14B relay.

It is postulated that the

momentarily sensed

decreased

EHC fluid pressure

caused the relay

contacts to open just long enough to de-energize

the sensitive

5A-

K14B relay.

~

The conditions resulted in about half of the Unit 2 SSPVs getting

an "electrical" scram signal

(channel

A t, scram

and the one relay

in the Bl channel).

This would cause the Group I and

IV rods to

get

a scram signal.

This theory also conforms with an Senior

Reactor Operator's

(SRO) observation that the Group I and

IV rod

groups

scram lights appeared to have actuated

before the other two

groups.

~

A "8" RPS side backup scram valve was energized

by, the 5A-K14B (in

conjunction with the half scram) which vented air off of the

control rod drive air header

and

a full scram was actuated.

The resident

inspectors directly observed portions of the

troubleshooting

and corrective actions.

Workers replacing the 5A-K14B

relay were attentive in their work and were utilizing good stop-think-

ask-and-act

techniques.

The inspectors

examined recorder

traces

which

supported

the licensee's

conclusions

regarding

EHC fluid pressure

oscillations

and relay performance.

Portions of testing of some of the

0

22

other

RPS relays were observed.

The inspectors

noted that the pressure

switches set point for turbine fast closure input to RPS were

conservatively

above the value specified in the Updated Final Safety

Analysis Report

(UFSAR).

One of the inspectors

attended

the restart Plant Operations

Review

Committee meeting

and noted that the II team

made

an effective

presentation

regarding the electrical

equipment

performance which caused

the scram.

The inspector

questioned if General Electric

(GE) had any

additional information regarding the

EHC pressure

spike theory and the

parallel

RPS relays not being actuated.

At the time, it was not known

if additional information was available,,but

management

indicated that

it was being pursued.

The II team also

recommended

several

long term

action items including development of stronger procedural

guidelines for

repairs of a control valve servo while at power.

Prior to restart,

the

licensee tested the other scram contactors

and did not identify any

problems.

A few days later,

a

GE engineer

noted that Service Information L'etter

(SIL) 508,

Scram Contractor Coil Life and Maintenance,

addressed

a

similar issue.

The SIL was issued in February

1990 and addressed

an

unexpected

scram at another Boiling Water

Reactor

which had been

caused

by some scram contactors

dropping out during very short duration scram

signals.

The inspector obtained

a copy of the SIL and the licensee's

documented

actions in response to the SIL.

The circumstances

involved

in the scram described

in the SIL appear to be very similar to the

Browns Ferry scram.

The SIL recommended that preventive maintenance

be

performed in the contactors

and that thei r service life be reviewed.

Documentation indicated that the Browns Ferry Unit 2 scram contactors

had been replaced in 1988 and thus would not be expected to be

approaching

end of service life.

The inspector

reviewed portions of

Procedure

EPI-099-RLY001,

and concluded that it addressed

the preventive

maintenance

recommended

in the SIL.

Licensee

Event Report

(LER) 260/97-007

was submitted to the

NRC on

November 25,

1997,

and addressed

the scram.

The

LER included

description of corrective actions to reduce

EHC pressure

decreases

during control valve movement through

EHC system modifications.

After startup of the unit, several

other incidents of control valve

servo leaks occurred

on Unit 2.

(A total of six servo leaks occurred

on

Unit 2 since startup after the refueling outage).

The leaks were

identified through careful monitoring of the

EHC tank levels.

In each

case,

power

was reduced

and the servos

were replaced.

The licensee

revised the repair

procedures

to include recommendations

from the II

team.

The inspector s verified that TS requi rements

were met during the

work activities which included installation of jumpers around pressure

switches with inputs into the Reactor

Protection

System.

The licensee

formed

a team which continued to investigate the cause of

the leaks.

The investigation included extensive testing of postulated

causes

and working with the servo vendors.

Subsequently,

the licensee

0

4i

23

determined the leaks were due to vibration or pressure oscillation

induced

movement of a servo port plug which was not secured sufficiently

to prevent the movement.

The plug movement

(a few mils) resulted in

degradation of an o'ring seal

and consequently

EHC oil leaked out of the

servo.

The leaking servos

had been replaced during the most recent

refueling outage with rebuilt servos.

The licensee indicated that the

servos

are rebuilt by two vendors which utilize different means of

securing the plug.

The plugs

on the leaking servos

were secured

in a

manner that .appeared to allow slight movement of the plug.

.At the close

of this report. the licensee

was attempting to procure replacement

servos of the type which seem to allow less plug movement.

For the

interim period, the licensee

has revised work instructions for servo

replacement

such that the plug will be more securely fastened.

Unit 3

also has the same type of servos installed but no leakage

has

been

detected.

Those servos apparently were from a different batch than the

Unit 2 servos.

The licensee is continuing to investigate the magnitude

and significance of vibrations .in the Unit 2

EHC system.

Work

instructions

have been

developed to install

a pressure

transducer

on

a

Unit 2 control valve during the next replacement that is performed.

The

device will monitor

EHC fluid pressure

at the control valves.

Problem Evaluation Report

(PER) 971714 described

the investigation

and'orrective

actions

regarding the

EHC leaks.

The

PER noted that

additional

EHC system modifications. including installation of

accumulators

and control valve manifolds,

are planned

as part of the

Power Uprate Project.

These modifications are referenced

in GE Turbine

Information Letter 1123,

issued

November

14,

1992.

The modifications are

intended to reduce

EHC fluid pressure oscillations.

Operations is

continuing to closely monitor

EHC reservoir fluid level

on both units.

The inspectors verified that the enhanced

monitoring is being properly

performed.

Conclusions

The inspectors

concluded that the l.icensee's

incident investigation

team

performed well in investigating the equipment

issues

which caused

the

scram.

The team studied available

information, developed

a theory of

the cause,

and in a prompt manner,

performed electrical testing which

supported the postulated

cause.

The investigation into the

EHC fluid

leaks

was also thorough

and determined the cause of the leaks in a

reasonable

time, period.

RCIC Lube Oil Particulate

Levels Increased

Ins ection Sco

e

37551

The inspector

reviewed data

and developed

a time line to assess

the

licensee's

actions in response to -high particulate levels in the Reactor

Core Isolation Cooling (RCIC) system lube oil.

Oil samples

indicated

a

articulate count which was in the action range

as identified by the

icensee's

procedures

and documentation in the vendor manual.

l

b.

Observations

and Findin s

24

On October 20.

1997,

a lube oil sample

was taken from the

RCIC system

following work which had been performed during the Unit 2 outage which

ended October

18,

1997.

Oil analyses

results

were issued

from the

licensee's

Central

Laboratory on October 22,

1997, which identified

a

particulate count of ISO 20/15.

On November 3,

1997, the licensee initiated a work request

C337743 to

sample the oil again to verify the high particulate content

and change

the oil if necessary.

On November 6,

1997, the sample

was taken to

verify Central

Laboratory results.

Browns Ferry laboratory determined

the particulate count,to

be high and that

an oil change

was required.

On November 21,

1997, the licensee

changed the oil in the

RCIC system.

Sampling following the oil change indicated

a high level of particulate.

The licensee

changed the oil and sampled for particulate levels several

times in an, attempt to decrease

particulate levels to within the normal

range.

Analyses of the oil sample taken from the RCIC system following

a 15 minute run on November 23.

1997,

showed

a particulate level of ISO

18/14 which placed the system in the Alert Range.

The Alert Range

requi res that the lube oil be filtered or replaced at the next refueling

outage if the alert limits persist.

On November

23,

1997, the licensee

declared the RCIC system operable.

Chemistry Instruction (CI) CI-130, Diesel

Fuel

and Lube Oil Monitoring

Program,

Revision

5

~ Attachment 3, describes

the RCIC lube oil

particulate guidelines.

The procedure

describes

three ranges:

Normal

Range

(ISO 16/13), Alert Range

(ISO 18/15),

and Action Range

(ISO

>18/>15).

The procedure states that the particulate counts which exceed

the alert range require immediate corrective action to be taken to

restore the oil to normal or alert levels.

The procedure further states

that the HPCI/RCIC system

may remain "functional" for a period not to

exceed

30 days while resampling / filtering / replacement activities are

in process.

The licensee

interpreted the procedural

requirements to

mean that the oil should

be changed within 30 days.

The RCIC,oil was

changed within thirty days of the date when the oil analysis results

were issued

from the licensee's

Central

Laboratory on October 22.

1997.

The licensee is in the process of developing guidance for the lube oil

program on site.

In inspection report 259,260,296/97-08.

the inspector

concluded that

weaknesses

in the licensee's

lubrication oil analysis

program permitted

the incorrect type of lubricating oil to be added to a second

EDG

several

months af'ter it had been installed in a different

EDG.

c.

Conclusions

Al.though the licensee's

actions to decrease

the oil particulate levels

in the

RCIC system were adequate,

the

RCIC oil particulate level issue

represents

another

example of the difficulties that the licensee is

II

E8

E8.1

25

experiencing with the lube oil analysis

program.

The licensee

has not

determined the cause of increased particulate but has determined it is

not due to excessive. bearing wear.

Miscellaneous

Engineering

Issues

(92902)

Closed

Ins ection Fol,low u

Item 50-'260 296/95-19-01:

reduced scope'of

valves in GL 89-10 program.

This item involved the licensee's

removal

of a number

of. valves from its GL 89-10 program.

The licensee's

actions

to resolve this item are discussed

in E1.3.b.1

above.

The licensee's

.

actions in returning valves to its program were satisfactory,

except

as,

addressed

by the violation described in that section of this report.

R2

R2.1

IV.

Plant

Su

ort

Status of Radiation Protection

and Chemistry Facilities and Equipment

Radi oacti ve Effluent Honitor Probl ems

Ins ection Sco

e

37551

71750

During review of operating logs, the resident inspectors

had noted

discussion of a problem involving the radioactive effluent monitor (0-

RH-90-130).

The inspector

questioned

resolution of the problem and the

'bsence

of a Problem Evaluation Report at

a subsequent

Management

Review

Committee

(HRC) meeting.

Several

days later, the problem occurred

again.

The inspectors

questioned

plant management

regarding the

problems

and the oper abi:lity status of the monitor .

The licensee

formed

an investigation team.

The inspectors

reviewed the regulatory

and

procedural

requirements

for the monitor,

examined the detector

and

associated

piping,

and monitored the licensee's

investigation.

b. Observations

and Findin s

The resident inspectors

noted that the October 21,

1997. operating

logs

described

an incident in which the radwaste

operators

had secured

an

effluent release after it was noted that the radiation monitor was

indicating an activity level which dropped to less than the background

level recorded before the release

began.

In accordance with the Offsite

Dose Calculation Manual, the monitor is required to normally be operable

during releases.

Releases

are permitted to be continued with an

inoperable monitor if compensatory

measures

are completed.

The release

was subsequently

restarted.

At a Management

Review Committee meeting,

the resident inspector questioned

the

resolution of the problem and .the

.absence of a Problem, Evaluation Report

(PER).

Subsequently,

maintenance

personnel

reported to the inspector that the problem had been attributed

to demineralized water remaining in the detector after

a cleaning

evolution.

C

0

26

On October 27, the problem occurred again.

The monitor was not declared

inoperable

and two releases

were made without compensatory

sampling

performed.

PER 971713 was initiated on October

28 to address

the issue.

After HRC review of this

PER on October 29. the inspector

questioned

the

operability status

of. the monitor since releases

were being

made without

completion of compensatory

measures

required

by the Offsite Dose

Calculation Manual

(ODCH).

The inspectors

also questioned

plant

management

regarding resolution of the problems.

The monitor was

declared

inoperable (administrative decision)

on October

29 and

compensatory

measures

were completed for all releases.

An Incident

Investigation (II) team was formed .to investigate the problems.

After some investigation,

the team identified that the problem was

caused

by water leaking out of the detector

housing

volume through

a

closed drain valve.

Maintenance

personnel

found an accumulation of crud

on the valve seat which allowed leakage

through the valve.

Drainage of

water out of the volume decreased

the shielding between the detector

and

the chamber walls.

When

a release

was started,

the volume was refilled

with low activity water and the radiation levels sensed

by the detector

wer e reduced.

The valve was replaced. and the licensee

subsequently

conducted testing .which supported

the postulated

cause.

During a

subsequent

release,

the decreased

radiation levels were not observed.

The investigation

team concluded that the RH-130 monitor had, in fact,

been functional despite the water draining problem.

The team also

verified that the

ODCM compensatory

measures

had been completed for all

periods in which the monitor had been inoperable.

The inspectors

reviewed portions of Technical

Instruction O-TI-45, Liquid Process

Radiation Monitors.

This procedure

determines

the alarm setpoints

as

required

by the

ODCH.

At Browns Ferry, 'liquid radwaste

batch discharges

are controlled by procedure O-SI-4.8.A, Liquid Effluent Permit.

Representative

samples

are analyzed prior to the discharge

and the

monitor serves

as

an independent

check during the discharge.

The

inspectors

noted

numerous

conservatisms

were applied, in the set point,

determinations

for 'RH-130, including conservative

assumptions

regarding

condenser circulating system (dilution) water flow.

After review of the

procedures

and discussions

with the team, the inspectors

concluded that

the decreased,

background effects observed

did not adversely affect the

.operability of the monitor.

On December

2,

1997, the .proposed corrective actions for

PER 971713 were

reviewed, by the Management

Review Committee

(HRC).

Initially, the

actions did not address

the inspector's principle concern that observed

abnormalities

associated

with the RM-130 were not fully understood

and

radioactive material

releases

were permitted to continue without

compensatory

measures.

During the

HRC meeting, the Site Vice President

directed that

a corrective action

be added which addressed

this concern.

The inspector discussed

the concern with the Operations

Manager

and

verified that the concern would be adequately

addressed.

\\

ll

0

c.

Conclusions

27

Unexpected indications

on the radioactive effluent monitor

recorder

were

not thoroughly investigated prior to discontinuation of compensatory

actions

required for an inoperable monitor.

The licensee

subsequently

completed

a detailed

investigation which identified that

a leaking

valve had caused

the unexpected

indications.

The investigation also

concluded that the monitor was not inoperable

and that regulatory

requirements

were met during, the period.

Xl

Exit Meeting Summary

V.

Mana ement Meetin s

The resident inspector presented

inspection findings and results to

licensee

management

on December

12.

1997.

Other formal meetings to

discuss

report issues

were conducted

on November

21,

and

December

3,

1997.

The licensee

acknowledged

the findings presented.

Proprietary

information is not included in this inspection report.

PARTIAL LIST OF

PERSONS

CONTACTED

T. Abney, Licensing Manager

J. Brazell, Site Security Manager

R. Coleman, Acting Radiological Control

Manage

M. Cooper,

Corporate

Component

Engineering

Manager

J.

Corey, Radiological Controls

and Chemistry

Manager

T. Cornelius,

Emergency

Preparedness

and Planning

C. Crane, Site Vice President,

Browns,Ferry

R.

Greenman,

Training Manager

J.

Johnson,

Site Quality Assurance

Manager

R. Jones,

Assistant Plant Manager

G. Little. Acting Operations

Manager

D.

Nye, Site Engineering

Manager

J. Schlessel.

Acting Maintenance

Manage

K. Singer,

Plant Manager

INSPECTION

PROCEDURES

USED

IP 37551:

IP 40500:

IP 62707:

IP 71707:

IP 71714:

IP 71750:

Onsite Engineering

Licensee Self-Assessments

Maintenance

Observations

Plant Operations

Cold Weather Preparations

Plant Support Activities

0

(

0

0

IP 9Z901:

IP 92902:

IP 93702:

TI 2515/109:

28

Follow up-Plant Operations

Follow up-Maintenance

Prompt Onsite Response to Events at Operating

Power Reactor

Implementation of Generic Letter 89-10

ITEMS OPENED

DISCUSSED

AND CLOSED

OPENED

~T

e

Item Number

IFI

260,296/97-11-01

VIO

260.296/97-11-02

URI

260,296/97-11-03

DEV

260,296/97-11-04

NCV

260,296/97-11-05

VIO

260,296/97-11-06

CLOSED

T~e

Item Number

VIO

.260/96-06-02

VIO

260/96-05-03

IFI

260,296/95-19-01

Status

Open

Open

Open

Open

Closed

Open

Status

Closed

Closed

Closed

Descri tion and Reference

Status

Control Issues

(Section 01.2)

Failure to Control

CREV Switch

Position (Section 01.3)

Adequacy of CREV Standby Train

Circuit Testing (Section 01.3)

Inadequate

Procedural

Controls for

MOV Activities (Section El.3)

Inadequate

Design Assumptions for

MOV Capability (Section E1.3)

Failure to Prepare the Trend Report

Required

by Procedures

(Section

El. 3)

Descri tion and Reference

Failure to: Perform

a 10CFR50.59

Evaluation Prior to Disabling

Annunciator

(Section 08. 1)

Customer

Group Workers

Exceeded

Overtime Limits Without Approved

Exemption (Section 08.2)

Reduced

Scope of Valves in GL 89-10

Program (Section E8.3)

k

'1

~QN

0

0

0