ML18038B944

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Insp Repts 50-259/97-08,50-260/97-08 & 50-296/97-08 on 970622-0802.Violation Noted.Major Areas Inspected: Operations,Engineering,Maint & Plant Support
ML18038B944
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 08/29/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18038B942 List:
References
50-259-97-08, 50-259-97-8, 50-260-97-08, 50-260-97-8, 50-296-97-08, 50-296-97-8, NUDOCS 9709040346
Download: ML18038B944 (94)


See also: IR 05000259/1997008

Text

U.S.

NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

License

Nos:

50-259.

50-260,

50-296

DPR-33,

DPR-52,

DPR-68

'Repor t Nos:

50-259/97-08.

50-260/97-08.

50-296/97-08

Licensee:

Tennessee

Valley Authority

Facility:

Browns Ferry Nuclear Plant, Units l. 2,

& 3

Location:

Corner of Shaw and Browns Ferry Roads

Athens.

AL

35611

Dates:

June

22 - August 2,

1997

Inspectors:

L. Wert, Senior Resident

Inspector

J. Starefos,

Resident

Inspector

C. Smith,

Reactor

Inspector

(Sections

E2.4,

E2.5.

and E8.5)

Approved by:

H. Lesser,

Chief

Reactor

Projects

Branch

6

Division of Reactor Projects

9709040346

970829

PDR

ADQCK 0500025'P

6

P,DR

Enclosure

2

0

il

EXECUTIVE SUMMARY

Browns Ferry Nuclear Plant, Units 1, 2,

8 3

NRC Inspection Report 50-259/97-08.

50-260/97-08,

50-296/97-08

This integrated

inspection included aspects

of licensee operations,

engineering.

maintenance,

and plant support.

The report covers

a six-week

period of resident inspection

and inspection in the engineering

area

by a

Region II reactor inspector.

Operations

management

promptly addressed

a power supply problem associated

with Anticipated Transient Without a Scram logic. Repairs

were completed in a

timely manner

and with effective Operations controls.

(Section 01. 1)

Control

room operators

demonstrated

an increased sensitivity to compensatory

actions for inoperable

equipment or instrumentation.

The actions were

conservative

and completed at reasonable

intervals.

(Section 01.2)

Housekeeping

deficiencies

were identified in the Unit 3 shutdown board

room

chiller rooms

and

a ventilation tower.

Overall conditions in the Unit 2

Reactor

Building were improved.

In the plant stack.

conditions were

satisfactory

and the radiation monitoring system

was aligned

as required.

(Section 02.1)

Monitoring of identified leakage

problems did not identify improperly rigged

catch devices or devices

which were not properly sized to capture

leakage.

While the overall status of temporary leakage

containment

devices

was

acceptable,

several of the devices

were not effectively capturing the leakage.

(Section 02.1)

The overall performance of the workers during Standby

Gas Treatment

System

testing

was good.

Workers were attentive to details of the testing

and good

0

procedural

compliance

was observed.

The maintenance

workers coordinated their

efforts with Operations.

The inspector identified that the surveillance

instruction did not fully address

orientation of the hot wire anemometer

sensor

probe during air flow measurements.

(Section Hl.l)

The Unit 2 High Pressure

Coolant Injection system

was affected by steam

admission valve leakage

condensate

entering

a junction box through an unsealed

conduit.

Surveillance testing indicated that the system

was capable of

performing its safety f'unction in the automatic

mode.

The valve steam leakage

problems

were known by the licensee

and had existed prior to the most recent

refueling outage.

The licensee's

detailed evaluation

focused

on effects of

valve seat

leakage.

The potential effects

due to external

leakage

were not as

fully evaluated.

The licensee's

actions,

including questioning of system

performance during the surveillance testing,

troubleshooting

and immediate

repair activities.

and planned future corrective actions were good.

(Non-

Cited Violation 50-260,296/97-07-03.

Failure to Identify Water Intrusion Into

High Pressure

Coolant Injection System Junction

Box. Section

E2. 1)

The inspectors identified that two steam packing exhauster line stack

isolation dampers

had been positioned differently than configuration control

drawings for approximately

one year to address

an equipment performance

issue.

The inspectors

did not identify any immediate safety concerns with the

equipment aligned in accordance

with the engineer's

instructions

and the

caution tag.

However, actions

had not been initiated to address

permanent

resolution of the problem.

(Section E2.2)

Weaknesses

iq the licensee's

lubrication oil analysis

program permitted'he

incorrect type of lubricating oil to be added to a second

'EDG several

months

after it had been installed in a different

EDG.

(Unresolved

Item 50-260/97-08-

02, Incorrect Oil.Used in Two EDGs, Section E2.3)

An error in the Haterials/Procurement

processes

resulted in workers procuring

the incorrect oil for addition to the

EDGs.

Similar examples of procurement

weaknesses

have, been identified previously.

The licensee

has initiated an

extensive Materials Upgrade Project to address

the issues.

(Inspection

Followup Item 50-260,296/97-08-05.

Materials Upgrade Project. Section

E2.3)

The licensee's

design control program was being implemented in accordance

with

the requirements

of ANSI N45.2. 11-1974.

(Section E2.4)

45

One violation was identified for failing to perform

a

10 CFR 50.59 Safety

Evaluation for a change to the

FSAR that permitted

a new system alignment that

previously had been prohibited by the licensing basis.

The deficiency

apparently involved misapplication of "S"

DCN which cannot

be used for making

system alignment changes.

Secondary

cause

was complex design control process

which uses

numerous

alphabet

designated

DCNs with unique administrative

controls.

(Violation 50-260/97-08-01,

Failure to perform a

10 CFR 50.59 Safety

Evaluation for New System Alignment, Section E2.4)

Technical Operability Evaluations

were technically adequate.

(Section

EZ.5)

Procurement

issues

involving Ellis and Watts

(Shutdown

Board

Room Chillers)

commercial dedication plans were adequately dispositioned for release of

material.

(Section E8.5)

The inspector

concluded that the licensee's

overall investigative

and

corrective actions regarding

a series of Emergency

Core Cooling System

inverter failures were effective.

The inverters continue to be monitored by

the licensee

as

an a(1) system in accordance

with the maintenance

rule.

The

failures

and corrective actions were well documented

in the licensee's

corrective action system.

(Section

E8. 1)

During observation of a compensatory

raw cooling water sampling activity

required by the Offsite Dose Calculation Hanual.

two deficiencies

were noted.

The worker did not fully comply with the sampling procedure.

The safety

significance of the specific deficiencies

was small since the overall intent

of the steps

was met.

Additionally, the Chemistry Shift Supervisor indicated

to the inspector that he was not aware of how the Lower Limit of Detection

acceptance criteria was met.

(Non-Cited Violation 259/97-08-04,

Failure to

Follow Chemistry Sampling Procedure.

Section

R4. 1)

0

0

4l

Unit 1 remained in a long-term lay-up condition with the reactor defueled.

Units 2 and 3 operated at or near full power with the exception of routine

testing

and scheduled

maintenance

downpowers.

Mhile performing the inspections

discussed

in this report, the inspectors

reviewed the applicable portions of the Updated Final Safety Analysis Report

(UFSAR) that related to most of the areas

inspected.

Section

E8.2 describes

a

minor UFSAR discrepancy identified during the reviews.

NRC review also

identified that

a safety assessment

contained

an incor rect statement.

(Section

E2. 1)

~

t

01

Conduct of Operations

01.1

The inspector

reviewed actions taken when Unit 3 experienced

a loss of

power to anticipated transient without a scram

(ATMS) B logic power.

The inspector

reviewed the licensee's

plan to repair the breaker.

observed

some of the repair activities,

reviewed the clearance,

and

observed

a portion of the equipment restoration.

On June 21,

1997, Unit 3 experienced

a loss of power to anticipated

transient without a scram

(ATWS) 8 logic power.

The licensee

determined

that the power interruption was caused

by a contact problem with normal

supply breaker

3-FUDS-248-3EBQ on the

3EB 250V

DC distribution panel.

The licensee cycled the breaker

several

times and verified that power

was restored to the

ATWS 8 logic panel.

Several

hours later, the

licensee transferred

ATMS 8 logic power to the alternate

power supply.

The licensee

performed shiftly voltage readings

on the normal supply to

0

ATWS B.

The inspectors

considered this to be an example of increased

sensitivity to compensatory

actions

by Operations

as discussed

in

Section 01.2.

On June 26,

1997, the licensee

removed the

3EB 250V

DC distribution

panel

from service to replace the 3-FUDS-248-3EBQ breaker.

The licensee

removed

a spare breaker

from another

part of the distribution panel

and

replaced the 3-FUDS-248-3EBQ breaker in accordance

with work order 97-

006508-000.

To remove the

3EB 250V

DC distribution panel

from service

for the breaker

replacement.

the licensee transferred

the 3EB 4160V

shutdown board control

power to.its alternate

supply, disconnected

the

3EB battery from the panel,

and disconnected

the

3EB battery charger

from the panel.

The ATMS B logic power was already transferred to its

alternate

power supply.

Technical Specification (TS) 3.9.B.6 requires

the licensee to notify the

NRC within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of the time that the 250V

shutdown board

3EB battery and/or its associated

battery board is found

to be inoperable for any reason;

continued reactor

operation is

permissible during the succeeding

seven

days.

The licensee

reported the

removal of the 250V shutdown board

3EB and the distribution panel

from

service

as required by TS 3.9.8.6.

The inspector

reviewed clearance

3-97-0507, verified that tags were hung

on equipment in the field. and that the equipment

was in its designated

clearance

position.

No concerns

were identified.

Following the breaker

replacement,

the licensee identified a problem with the physical

interlocks which keep the'panel

door closed

when the breaker is closed.

During troubleshooting

work, the inspector noted that

a number of the

breakers within the clearance

boundary were manipulated.

The inspector

discussed this with the tagging

SRO and

a component verification sheet

was prepared f'r designated

breakers

on the panel.

Operations

management

promptly informed the resident inspectors of the

problem with the normal..supply breaker

and their plan to effect repairs.

The repairs were completed in a timely manner

and with effective

Operations controls.

One of'he inspectors

observed Assistant Unit Operators

(AUOs) in the

diesel

generator

room during surveillance instruction (SI)

3-SI-4.9.A. l.a(3B), Diesel Generator

3B Monthly Operability Test.

The inspectors

reviewed the compensatory

actions initiated by the

control

room personnel

for inoperable instrumentation or equipment.

The inspectors verified that proper actions

were completed

when

important electrical

equipment

was placed in an alternate

alignment.

On July 20,

1997, the inspector observed

performance of surveillance

instruction 3-SI-4.9.A.l.a(3B), Diesel Generator

3B Monthly Operability

Test,

Revision 28.

The inspector attended

the pre-job briefing prior to

the test

and noted that the workers were told to ensure that they were

on the right component.

Discussion with the

AUO regarding draining

condensate

from the fuel oil day tank indicated that the

AUO was

knowledgeable of how to properly perform the activity.

The AUO

demonstrated

the technique to verify that the control cabinet

f'an was

operating.

In general,

observed

AUO performance

was good.

The inspector noted that several

steps of a section of the procedure

were performed before the preceding step

was signed off.

The inspector

observed that the procedure

steps

were being completed in order and that

the oversight

was administrative.

As discussed

in Inspection

Report

50-259,260,296/97-07,

similar practices

have

been previously noted

and

licensee

management

is reviewing the guidance currently set forth in

SSP-2.1,

Site Procedures

Program for signing off steps of continuous

use

procedures.

Over the last several

months.

the inspectors

have noted

an increased

sensitivity toward implementing compensatory

actions for plant equipment

problems.

Examples

included monitoring of 3B drywell control air

compressor

oil level due to 3A drywell control air compressor

being out

of service,

generator

PCB 234 cooling water conductivity monitored due

to annunciator disabled,

south emergency

equipment cooling water header

pressure

monitored due to a pressure transmitter being inoperable,

and

Unit 2 recombiner

room temperature

monitored

due to annunciator

alarm

0

il

disabled.

In general.

the control

room operators

exhibited more

sensitivity towards

compensatory

actions than was observed

during

previous inspections.

The inspectors

reviewed

an evolution in which control

room operators

were required to calculate transformer loading and observe

unusual

restrictions in an off-normal electrical switchgear alignment.

A

related potential .concern regarding this is discussed

in Section

E2.5 of

this report..

On July 24,

1997. the

2B 480

V Shutdown

Board was placed

on its "alternate" supply to support transformer work.

This invoked

several

special

operating restrictions

and necessitated

calculation of

loading by the operators.

The inspectors

reviewed the applicable plant

drawings

and instructions to determine the appropriate actions.

The

inspector verified that the restrictions

had been

met and that the

operators

performed the calculations correctly.

Two SROs in the Unit 2

control

room were able to explain the loading calculations

and had

performed

them correctly.

The inspectors

concluded that the

calculations

were not unreasonably difficult for the operators to

perform.

The work and the methods to meet the alignment restrictions

were planned through Maintenance

and Engineering

and set forth in a

detailed "fragnet" before the board alignment

was revised.

General

observations

during the report period were positive.

Control

room. operators

demonstrated

an increased sensitivity to compensatory

actions

when equipment or instruments

were inoperable.

Operators

successfully

performed calculations to meet special

operating

restrictions

due to an off-normal electrical switch gear

alignment.

02

Operational

Status of Facilities and Equipment

02.1

1

In addition to routine plant tours, the inspectors

reviewed installed

temporary leakage

containment

devices

and performed

a detailed tour of

the plant stack.

The stack tour specifically focused

on dilution

fans/dampers

and the stack radiation monitoring system.

il

0

On July 23, the inspectors

walked down the plant stack,

focusing on

operability of the dilution fans/dampers

and the stack effluent

radiation monitoring equipment.

Valves were positioned

as described

on controlled drawings with one

exception.

Section

E2. 1 of this report describes

review of a steam

packing exhauster

bypass line damper which had been caution tagged shut

since August 1996.

Several

valves were locked in position which the

Mechanical

Control drawing did not specifically require to be locked.

The inspectors

confirmed that the valves were appropriately listed in

the Operating Instructions.

Although some areas

.had large quantities of

insects

present,

overall housekeeping

conditions in the stack were

acceptable.

Material was properly stored with no excessive

accumulation

of equipment.

The radiation monitoring system

was aligned

as required

and appeared to be functioning properly.

The inspector noted that valve 2-65-513 (isolation valve in dilution

line to Standby

Gas Treatment

system header)

was incorrectly listed on

drawing 2-47E610-66-1

R024 as 3-65-513.

The licensee initiated

a

Problem Evaluation Report

(PER) to address this issue.

Early in the inspection period. the inspector.

noted poor housekeeping

conditions in the Unit 3 shutdown board chiller rooms.

The conditions

were corrected later in the inspection report period but the floor

drains in the rooms remained

clogged.

The inspectors

also noted

a pile

of high efficiency particulate filters in one of the vent towers above

the control building.

The filters were subsequently

removed from the

tower.

On July 16,, 1997,

one of the inspectors

examined

a sampling of

identified leaks

and leakage

containment

devices throughout the plant.

Condensation

from an identified steam packing leak on the Unit 2 High

Pressure

Coolant Injection (HPCI) system leaked into a junction box and

affected the HPCI control system (Section

E2. 1).

At the time, the

licensee

was tracking 27 non-contaminated

and 34 contaminated

temporary

'eakage

containment

devices.

The inspector

reviewed

14 of the non-

contaminated

leakage

devices.

Only one deficiency was noted.

Device

number 25, associated

with a recirculation

pump oil system leak,

was not

capturing all of the leaking oil and oil was running down adjacent

structural material.

The inspector

reviewed

16 of the 34 leakage

containment

devices for contaminated

systems.

Problems were noted with

II

five of the temporary devices.

Several

devices

were not effectively

capturing the leakage

due to undersized

devices

or not properly rigged

devices.

Plant management

was informed of the observations.

Subsequently,

the inspectors

noted that the observed

problems

had been

corrected.

The licensee tracks temporary leakage

containment

devices

and an updated list is reviewed each

week at the Plan of the Day

meeting.

The licensee

does not have

a formal process

which would ensure

specific regular or periodic review of the installed devices.

The

licensee relies

on routine Operations tours or system engineer

observations

to monitor identified leakage

problems.

Housekeeping

deficiencies

were identified in the Unit 3 shutdown board

room chiller rooms and

a vent tower.

With the exception of chiller room

floor drain blockage,

those issues

were corrected during the inspection

period.

In the plant stack, material

was properly stored

and there was

not an excessive quantity of stored equipment.

The radiation monitoring

system

was aligned

as required

and appeared to be functioning properly.

Licensee monitoring of identified leakage

problems did not identify

improperly rigged catch devices or devices which were not properly sized

to capture

leakage.

While the overall status of temporary

leakage

containment devices

was acceptable,

several of the devices

were not

effectively capturing the leakage.

08

Hiscellaneous

Operations

Issues

(92901)

08.1

l

, Core Thermal

Power

Exceeded

Operating License's

Haximum Power Level

Due to a Drifting

Temperature Transmitter.

Violation 296/96-01-01,

Core Thermal

Power

Above Licensed Condition Haximum. also addressed

this issue.

The

licensee's

corrective actions

were reviewed

and the violation was closed

in Inspection Report (IR) 96-04.

The IR noted that the licensee

completed several. corrective actions which were not listed in the

response

to the Notice of Violation.

The inspectors

continue to observe

that the Unit Operators

are informing the Unit Senior Reactor Operator

of recirculation flow changes.

The

LER is closed.

08.2

V

- 4-, Fire Protection

Program Equipment

Inoperable Without Compensatory Actions.

This violation addressed

two

examples in which required compensatory

actions

were not initiated for

inoperable fire protection program

equipment.

An improper clearance

il

rendered

a reactor building preaction sprinkler valve inoperable

and an

inoperable battery charger switch was not recognized

as fire protection

equipment.

The licensee

has strengthened

the processes

used to develop

and review clearances

since this event

and no similar incidents

have

occurred.

The second deficiency occurred

due to a vendor wiring error

in the control panel for.'the battery charger.

Since

1986, the licensee

has

had procedural

requirements

for wiring verification of new vendor

wired electrical

equipment.

No additional

examples of such problems

have been noted.

NRC checks of fire protection program compensatory

measures

have not identified any problems in recent

months.

Hl

Conduct of Haintenance

Hl.l

Utilizing -the guidance of Inspection

Procedure

61726, the inspector

obser ved major portions of five surveillance tests

conducted

on the "C"

train of SBGT.

0-SI-4.7.8.1. 8-3

O-SI-4.7.8.3-3

O-SI-4.7.8.1.A-3

O-SI-4.7.8.7

O-SI-4.7.8.8

"C" SBGT Humidity Control Heater Test

"C" SBGT Flow Distribution Test

"C" SBGT Filter Pressure

Drop Test

"C" SBGT Flow Rate Test

"C" SBGT Housing Door Gasket

Seal

F

During the per iod of July 9-11.

1997, the inspector observed testing of

the

SBGT system

as required by technical specifications

(TS).

In

preparation,

the inspector

reviewed controlled drawings

and

UFSAR

descriptions of the system.

walked down portions of the

SBGT system,

and

reviewed operating

and testing procedures.

The inspector

observed that the humidity heater

control testing

was well

controlled, with close utilization of the procedure.

The inspector

observed that torquing of'he dyoctlphosphate test port flanges

was

performed properly with Quality Control involvement

as required

by the

procedure.

The inspector noted that mechanical

maintenance

workers coordinated with

Operations to obtain .permission to begin testing

and ensure that the

prerequisites

were met f'r the other four tests.

The workers were also

diligent regarding signing off the initial steps in the procedure

as

they were completed.

The workers

had marked the pitot tube and the hot

wire anemometer

tube with tape to expedite traverse point measurements.

During the

SBGT flow rate test,

two 20 point pitot tube traverses

were

obtained

from SBGT piping located in the plant stack.

The inspector

observed that the workers attempted to be accurate

and consistent

regarding

manometer

data.

The inspector

recorded

manometer

readings

and

performed the calculations of SBGT train flow independent of the

workers.

The inspector obtained flowrate values very close to the values

the workers obtained

and well within the acceptance criteria.

The uniformity of air distribution across

the High Efficiency

Particulate Air (HEPA) filters and charcoal

adsorbers

is required to be

checked

by TS 4.7.B.l.c.

Procedure

O-SI-4.7.B.3-3,

"C" SBGT Flow

Distribution Test, is used to perform this testing.

A hot wire

anemometer

is utilized to obtain

a nine point velocity profile on the

upstream

HEPA filter.

During the testing,

the inspector

observed that

rotation of the probe with respect to air flow affected the readings

obtained.

At one point,

an initial reading

was lower than the expected

value.

After obtaining the other two points in that column, the workers

'obtained

another

reading at the first point which was close to the other

two point values.

By referring to a piece'f tape

on the probe tube

extension,

the inspector noted that the orientation of the tube had been

changed

between the readings.

At the inspector's

request.

the workers

rotated the probe ninety degrees

at another point and it was confirmed

that the orientation of the probe affected the readings.

Although some

discussion

was held on the orientation of the probe, the workers did not

indicate that they. were aware of the significance of probe orientation.

Subsequently.

the inspector

reviewed the instruction manual

supplied by

the instrument vendor.

The manual stated that

a red dot painted

on the

-

end of the probe was to be toward the air flow to obtain valid readings

The inspector confirmed that there

was

a red dot on the probe

as

specified.

Discussions with maintenance training personnel

indicated

that the probe orientation was briefly addressed

during training

sessions

with the workers.

The inspector noted that the probe only

extends to 21 inches

and. the workers have to attach the probe to an

extension tube to extend it far enough into the train.

This increases

the difficulty in ensuring that the, probe is, oriented properly.

These

observations

were reported to plant management.

0

The licensee

subsequently

concluded that the performed SI was

acceptable.

However, the test procedure

was revised to require that the

maximum indicated flowrate (as the probe. is rotated)

be recorded at each

measurement

point.

The inspector concluded that this would provide

a

more accurate

assessment

of flow distribution within the train.

Additionally. the plant manager

informed the inspector that his

investigation indicated that the workers were aware of the significance

of probe orientation but had apparently not communicated their knowledge

to the inspector.

The inspectors

concluded that the licensee's

revision

to the procedure

adequately

addressed

the issue

and strengthened

instructions. to the workers regarding air flow measurements.

The

inspectors

did not identify reasonable

conditions where improper

probe

orientation would have failed to identify inadequate

air flows.

The SBGT Filter Drop Test and Housing Door Gasket

Seal Test were

completed satisfactorily

and results

were .within acceptance criteria.

During reviews of the SBGT system,

the inspector identified that the

Unit 3 control

room mimic had manual

bypass

decay heat line damper

DMP-

65-02 labeled

as

DMP-65-21.

This was reported to Operations

management.

The inspector subsequently verified that the control

room mimic was

corrected.

The overal,l performance of the workers during the testing

was good.

Workers were attentive to details of the testing

and good procedural

compliance

was observed.

The maintenance

workers coordinated their

efforts with Operations.

The inspector identified that the surveillance

instruction did not fully address orientation of the hot wire anemometer

sensor

probe during air flow measurements.

One minor deficiency

involving a control

room mimic display was noted.

The inspector

obser ved the performance of Surveillance Instruction

2-SI-4.1.A-8(F),

RPS High Water Level in Scram Discharge

Tank Functional

Test 2-LS-85-45E and 2-LS-85-45F,

Revision 12.

0

il

On July 8.

1997, the inspector

observed the performance of Surveillance

Instruction 2-SI-4. 1.A-8(F),

RPS High Water Level in Scram Discharge

Tank Functional Test 2-LS-85-45E

and 2-LS-85-45F,

Revision 12.

The

inspector observed portions of the SI from the cage

area

around the east

scram discharge tanks,

from the control

room,

and from the Unit 2

auxiliary instrument

room.

The individuals performing valve

manipulations in the field exercised clear communications

and verified

the correct components

before manipulation.

Second party verification

and independent verification was adequate.

During the performance of the testing,

the inspector

noted that the

individuals performing the test were careful to control

a test valve by

attaching it to the area

cage.

During previous testing,

water had

leaked by the valve causing

a half-scram (IR 97-01, Section M4.1).

In

addition, the inspector noted that the licensee

enhanced

the SI

procedure

by adding

a step to close the demineralized

water source

connection valve which provides

a second isolation between the manometer

and the water supply.

M8

Miscellaneous

Maintenance

Issues

(62707,

92902)

M8.1

, Failure to Follow Procedures

During

Core Spray Valve Maintenance.

NRC inspectors identified that

maintenance

workers were not signing off completion of steps

as the work

was completed.

Plant management

has continued to emphasize

%hat

procedural

steps

are to be completed

and,

when required,

signed

as the

steps

are completed.

Recently. the inspectors

have noted that

"continuous

use" procedures

are being revised to support step completion

documentation at appropriate locations in the procedure.

The inspectors

have noted overall

improvement in maintenance

workers signing off

prerequisites

or major steps

as they are completed.

However,

some

procedures

are not written in a, manner to support rigid step-by-step

signoffs.

Section Ml.1 of Inspection Report 97-07 describes

NRC

observation of Common Accident Signal. Testing in which workers completed

small groups of steps

before stopping to sign steps.

The steps

were

performed correctly and in sequence.

The inspectors

have observed

plant management

discuss

the issue of completion signoffs in Management

Review Committee meetings.

Procedures

are being revised

as

enhancement

areas

are identified.

Section Ml. 1 of this report describes

testing

observations

in which it was noted that the workers were sensitive to

sequential

step completion.

The violation is closed.

Cl

0

M8;2

. Licensee Identified Appendix

R

Deficiencies.

This violation addressed

several

Appendix

R issues

identified during extensive re-analysis of the Unit 2 safe

shutdown

program.

The Notice of Violation stated that no response to the

violation was required since the licensee

had adequately

addressed

the

issues

in Licensee

Event Report

(L'ER) 260/96-001.

Revision I of the

LER

was closed in IR 96-08.

The licensee thoroughly reviewed each of the

deficiencies

and concluded that no consistent

trend or methodology

problems were involved.

The inspector

reviewed documentation

which

indicated that modification F39514A had been completed which re-routed

several

instrumentation

cables to correct the problems.

The other

corrective actions in the

LER were completed

as well.

The violation is

closed.

M8.3

,

10 CFR Part 50

Appendix

R Noncompliance Results in the Plant Being Outside Its Design

Basis

and Being in a Condition Not Covered

by Plant Operating

Instructions.

Section

M8.2 describes

review of a violation which

addressed

the issues

in the

LER.

Revision

1 of the

LER was closed in IR

96-08.

Due to an administrative oversight,

Revision

0 was not closed at

that time.

The

LER is closed.

M8.4

, Toolpouch

Issues.

This URI contained

two central

issues.

The first issue

was

adequacy of the toolpouch maintenance

process for work on the emergency

diesel

generators

(EDGs).

The second

issue involved weaknesses

in the

procurement

processes

which could have allowed improper material

(glycol) to be added to the

EDGs.

The licensee

completed

an evaluation of whether the Toolpouch

Maintenance, process

was appropriate

for adding demineralized

water to

the emergency diesel

generators

cooling systems.

The licensee

determined that the toolpouch criteria and examples,

described in site

standard practice

(SSP)

procedure

SSP-6.2

(Maintenance

Management

System)

Appendix T (Implementing Toolpouch Maintenance),

could not be

used effectively to determine toolpouch maintenance

items.

Problem

Evaluation Report

(PER)

BFPER961761

addressed

this issue with an update

to procedure

SSP-6.2 Appendix T.

Craft supervisors,

foremen,

and

maintenance

planners

were briefed on the revised procedure

appendix.

The inspector

reviewed SSP-6.2 Appendix T, Revision 26.

and concluded

that the procedure .would currently not allow demineralized water

-addition to the emergency diesel

generators

cooling systems

using the

Toolpouch Maintenance

Process.

Due to another

problem that occurred involving the

EDG coolant expansion

tank, the licensee

developed

an operations

plant information posting

(PIP-97-179)

and installed it at each diesel

informing personnel

to

contact chemistry for any additions,

sampling,

or chemistry concerns.

Based

upon the licensee's

actions to clarify the procedure

for Toolpouch

Maintenance,

to inform responsible

individuals of the changes,

and

installing Plant Information Postings at each diesel.

the inspector

concluded that this portion of the Unresolved

Item is closed.

No

violation of regulatory requirements

was identified.

0

The second part of the URI identified the potential for ethylene glycol

to be issued

by TVA Power Stores for use in the Emergency Diesel

Generators.

(EDGs) despite the fact that Site Standard

Practice

SSP-13. 1,

Chemistry Program,

does not consider ethylene glycol as acceptable for

use in the

EDGs.

This portion of Unresolved

Item 50-259,260.296/96-13-

02 will be addressed

by Inspection Followup Item (IFI) 50-260.296/97-08-

05, Materials Upgrade Project.

This IFI is addressed

in more detail in

Section

E2.2 of this report.

Unresolved

Item 50-259,260,296/96-13-02,

Toolpouch Issues is closed.

E2

Engineering Support of Facilities and Equipment

E2.1,

Condensation

from a steam leak on the Unit 2 High Pressure

Coolant

Injection (HPCI) system

steam admission valve entered

an electrical

junction box and affected the HPCI system.

The inspectors

monitored the

licensee's

efforts to troubleshoot

and correct the problem.

The

inspectors

reviewed the licensee's

controls regarding junction box

0

sealing.

The inspectors

reviewed electrical wiring and

HPCI control

system drawings

as well as test data to verify the impact of the water

intrusion on the

HPCI system.

On July 11,

1997, during the performance of surveillance

instruction

(SI) 2-SI-4.5.E.l.d,

HPCI fHigh Pressure

Coolant Injectionj Flow Rate

Test at Normal

RPV fReactor

Pressure

Vesselj Pressure,

the HPCI system

did not meet the SI requirements

while the system

was in manual

mode.

The testing indicated

an acceptable

flow (5050 gpm). at

a discharge

pressure

capable of vessel

injection (1210 psig)..

The Unit 2 HPCI

system

was declared

inoperable f'r troubleshooting

and corrective

actions.

The licensee

reported the condition to the

NRC.

The

inspectors

observed portions of the troubleshooting activities and

monitored the licensee's

investigation into the cause of the problem.

Initial troubleshooting identified a problem with the speed indicator

card in the

EGN portion of the turbine governor.

The licensee

replaced

the speed indicator card and reperformed the surveillance test.

The

testing indicated similar results with a small

improvement in indicated

performance.

Erratic indications were noted when the speed control

potentiometer

on the

HPCI speed controller was touched,

indicating

ground problems.

The licensee

was concerned that the ground on the

speed controller may have

damaged

the speed indicator card,

so it was

replaced

a second time.

Additional troubleshooting identified that the

output of the speed control potentiometer

on the HPCI speed controller

was erratic.

After correcting the apparent

problems,

the licensee

ran

the SI again

and determined that the symptoms still existed.

Further

troubleshooting identified that

a ground existed in the circuit which

was traced to junction box 8272 on the HPCI skid.

Additional inspection indicated that water was leaking into junction box

8272.

This is

a junction box located adjacent to the

HPCI turbine skid

which contains

a terminal board

and electrical

connections.

On July 14.

1997,

one of the inspectors

observed the inspection

and repairs to the

junction box in accordance

with Mork Order 97-007072-000.

The inspector observed that water was entering the junction box and

essentially all the terminal points

on

a large terminal strip inside the

box were wet.

Corrosion was evident

on many of the connections.

The

inspector traced the source of the water

and determined that it was from

a packing leak on the 73-16 valve

(HPCI steam admission valve).

0

Condensed

steam

had accumulated

in insulation on piping. then dripped

out the other side of the insulation

on

a nearby pipe elbow and finally

dripped

on the top of the junction box.

.The water entered the box

through two unsea1ed

conduit connections

on the top of the box and ran

down the terminal strip.

The inspector noted that the leakage into the

box was difficult to observe.

There was not

a visible puddle

on top of

the box and the path of condensate

from the 73-16 steam

leakage to the

box was torturous (the steam

was not simply condensing

on

a nearby

surface

and dropping into the box).

The terminal strip was replaced,

the conduit connections

were sealed

with an approved sealant material,

and the 73-16 steam leak condensation

was routed to a drain.

The inspector

observed that the workers were

careful

about component verification prior to beginning work and

utilized procedures

to track configuration

as wi res were lifted and

reconnected.

The 73-16 internal

leakage

issues

had been identified on both Browns

Ferry units as early as

1994.

Engineering

has

been pursuing corrective

actions,

including a modification which would replace the valves, with

an improved design in a vertical orientation.

A management

decision

was

made to not replace the valve during the last refueling outage.

Technical Operability Evaluation

(TOE) 2-94-073-9014,

Unit 2 HPCI Steam

Admission Valve Leakage

Problems.

had been written to address

the

leakage

and related issues.

The

TOE has

been updated several

times

since the original version.

The current revision, Revision 4, is

a

highly detailed

assessment

of the degraded condition.

The Senior

Resident

Inspector

had reviewed the

TOE and discussed

the issues with

the

HPCI system engineer previously.

The

TOE thoroughly addressed

issues

associated

with leakage

past the seat of the valve.

The

TOE

addressed

external

leakage

impacts briefly from the perspective of room

temperature.

The inspectors

reviewed the licensee's

controls regarding sealing of

junction boxes

and concluded that there are two basic methods for

controlling the sealing of the boxes:

~

Drawing 0-45B891-1,

Coqduits

and Grounding Waterproofing

and

Sealing.

Details of Electrical

Equipment,

provides guidance

regarding sealing of junction boxes.

Note 2 of the drawing

states:

"Seal conduits

and boxes in the reactor building, control

bay,

pumping station,

and diesel

generator buildings in accordance

with notes

3 thru 9.

See Drawing 0-45E491-31

for list of junction

0

0

~f

boxes that are required to be sealed."

Junction

box 8272 is not

listed on drawing 0-45E491-31.

Note

1 on Drawing 0-45E491-31

states:

"Listed are the Unit 1,

2. and 3 and

common area

enclosures

which contain electrical

components that require

moisture protection.

Seal

these

boxes according to requirements

on. Drawing 45E891-1."

Terminal or connection

boards

are not

normally considered

as

components that would require sealing.

The

junction boxes that are required to be sealed contain

environmental qualification sensitive electrical

equipment.

~

Attachment

5 of Procedure

EII-O-OOO-TCC106, Troubleshooting

and

Configuration Control of Electrical

Equipment contains

guidance

for resealing of conduit boxes

opened during performance of'he

troubleshooting

procedure.

Page

2 of the attachment

contains

specific guidance for junction box sealing

and drainage hole

verification.

Page

1 contains

a note "per drawing 45B891."

As

described

above.

since

JB 8272 is not listed on the drawing,

these instructions would not result in the JB being sealed after

work was completed in the box.

The inspector

had observed that it is

a

common work practice at Browns

Ferry to thoroughly seal junction. boxes after work .activities are

completed, if the box was found sealed,

including some boxes not listed

on 45E491-31.

In most cases.

similar boxes

have conduits with

watertight threaded

conduit boss

hubs

or the connections

are sealed with

an approved sealant.

The inspectors

noted that the conduit connections

on the identical junction box on Unit 3 HPCI appeared to be sealed

but

no drainage hole is present.

The inspector

reviewed the history associated

with the licensee's

processes

for junction box and conduit sealing.

In August 1987, water

was introduced into the scram discharge

instrument

volume

instrumentation

through

an unsealed

conduit after an inadvertent fire

suppression

system actuation.

A Notice of Violation was issued in

Inspection

Report 87-33 on this issue.

Condition Adverse to Quality

Report

(CAQR)

BFN 870913 was initiated.

Initially, the licensee's

planned corrective actions included sealing of all junction boxes in the

intake structure,

control bay. reactor building.

and diesel

generator

building.

In an October

17,

1991. letter to the

NRC.

TVA revised the

commitment.

An evaluation of plant areas

subject to moisture intrusion

and required to support Unit 2 operations

was performed.

TVA identified

areas

where conduit and junction boxes could be subjected to

condensation

from moderate

and high energy line breaks

and from open

16

head fixed water spray fire protection systems.

The list of junction

boxes to be sealed

was reduced.

The violation was closed out in

IR 91-16.

The inspectors

reviewed plant instructions,

design specifications,

and

drawings regarding the

HPCI room junction boxes.

The inspectors

concluded that the boxes are not required to be included

on the list of

junction boxes to be sealed:

~

Drawings 47W225-103

and -104 address

the harsh environmental

data

for the Unit 2 HPCI room.

The High Energy Line Break

(HELB)

profiles indicate that the HPCI room is not considered

a harsh

environment for any HELB scenarios

except for a line break in the

HPCI room itself.

Since

a

HELB in the HPCI room would involve the

HPCI steam piping. the HPCI system is not expected to perform in a

harsh environment.

The fire protection systems

in the Unit 2 and Unit 3 HPCI rooms

were converted to closed

head

systems prior to each unit restart.

In addition, to actuate the local spray device,

a heat detector

must actuate

a preaction valve to initiate water

spray to the

nozzles.

As such,

HPCI room junction boxes would no longer be

considered

as vulnerable to moisture intrusion from inadvertent

fire suppression

system actuation.

The inspector's

review also identified that Inspection Followup Item 84-

41-04 indicated that the licensee

had previously identified

a need to

relocate the HPCI

EGN control box.

Due to high moisture

and

temperatures,

the licensee

implemented

ECN P3184 which moved the

controls from adjacent to the

HPCI turbine (in JB 8272) to a location on

a

HPCI room wal.l.

.(Earlier work by General Electric had preliminari ly

indicated that the HPCI room would be

a harsh environment,

but this was

later revised).

The inspectors

reviewed portions of the

ECN package

and

did not identify any requi rements to seal. JB 8272 during the work.

In LER 260/97-003-00,

the licensee stated that the HPCI system could

have performed its function (prior to being

removed from service f'r

repairs).

The inspectors

reviewed electrical

drawings

and test data

and

concluded that the information supported

a conclusion that the

HPCI

system

was operable.

The observed

problems were due to the water

affecting the speed indication/control circuit which did not affect HPCI

as far as automatic startup

and injection.

The inspectors

noted that

the water and corroded terminations could have affected automatic

0

injection.

had this condition persisted,

since

some of'he wetted

terminations

are associated

with the

EGM control circuitry.

10 CFR 50,

Appendix 8, Criterion XVI. requires that. measures

shall

be established

to assure that conditions adverse to quality. such

as failures.

malfunctions, deficiencies.

deviations,

defective material

and

equipment,

and nonconformances

are promptly identified and corrected.

In

this case,

Unit 2 High Pressure

Coolant Injection system controls were

affected

due to steam admission valve leakage

condensate

entering

a

junction box through unsealed

conduit.

The valve steam

leakage

problems

were

known by the licensee

and had existed prior to the most recent

refueling outage.

The licensee's

detailed evaluation

focused

on effects

of valve seat

leakage

and potential effects

due to external

leakage

were

not as fully evaluated.

Although several

factors

made it difficult to

see the leakage into the junction box, the degraded

condition was not

identified until after

HPCI was affected.

Conditions inside the

junction box indicated that water had been entering the box for several

months prior to identification.

Corrective actions include:

HPCI was declared

inoperable

and after

some troubleshooting,

traced the cause to water entering the box.

The damaged terminal

strip was replaced.

the box was sealed.

Leakage containment

around the 73-16 valve was improved.

All installed. "leakage containment

devices"

(the devices

are

numbered

and tracked)

were examined to ensure that no other

similar problems existed.

Walkdowns of HPCI.

RCIC.

and feedwater

pump rooms where steam

condensate

could leak on junction boxes will be performed.

Conduit terminations would be sealed

on those

deemed to be

unacceptable.

Training modules will be developed to address this event

and

management

expectations

on reviewing aff'ects of plant leaks

and

the reporting of such leaks.

A Site Bulletin will be issued to heighten

awareness

of plant

personnel

to this event.

il

0

The inspectors. concluded that the licensee's

corrective actions

are

adequate.

The condition was identified by the licensee

as

a result of

questioning during the performance of surveillance

testing.

Although

available

information indicates that the

HPCI system could have

performed its intended safety function during the testing,

the condition

was adverse to quality and was not promptly identified.

This l.icensee-

identified and corrected violation is being treated

as

a Non-Cited

Violation (NCV), consistent with Section VII.B.1 of NRC Enforcement

Policy.

(NCV 50-260/97-07-01,

Failure to Identify Water Intrusion Into

High Pressure

Coolant Injection System Junction Box).

The Unit 2 High Pressure

Coolant Injection system

was affected

by steam

admission valve leakage

condensate

entering

a junction box through

unsealed

conduit penetrations.

The valve steam leakage

problems were

known by the licensee

and had existed prior to the most recent refueling

outage.

The licensee's

detailed evaluation

focused

on effects of valve

seat

leakage

and potential effects

due to external

leakage

were not as

fully evaluated.

The inspectors

concluded that three key issues

played

a role in the HPCI

control system being affected prior to identification of the problem.

Effects of longterm external

valve leakage

were not evaluated in a

sufficiently detailed

manner to identify the leakage into the junction

box. Identified long-standing valve leakage conditions were not

periodically evaluated

by means other than routine rounds.

Some

electrical junction boxes adjacent to steam operated

equipment

are not

sealed

against moisture intrusion.

The licensee's

actions.

including questioning of system performance

during the surveillance testing, troubleshooting

and immediate repair

activities,

and planned future corrective actions were good.

mP

During a tour of the plant stack

on July 23,

1997,

(Section 01.2) the

inspectors

noted that caution tag 0-96-0355-1

was present

on damper 0-

DMP-66-953A.

The tag had been installed in August 1996 and stated that

the damper

was to be shut.

Since the controlled drawings indicated that

~

i

0

the damper

was to be open

and the tag had been in place for almost

a

year, the inspectors

reviewed the damper position and caution tag issues

more closely.

Caution Tag 0-96-355-1 stated that 0-DMP-66-953A was to remain shut.

Two isolation dampers

(0-DMP-66-953A and 953B) are located in a pipe

from the steam packing exhaust to the stack

[Steam Packing Exhauster

(SPE)

bypass linej.

Two backdraft

dampers

are located between the

isolation dampers.

There is an. additional set of isolation dampers

and

backdraft

dampers

in parallel with this line.

The inspectors

noted that

Configuration Control Drawings 2-47E809-2

(Revision 21) and 2-47E610-66-

I indicated that the bypass isolation dampers

were to be open.

Note 11

on 2-47E809-2 stated that air flow was required to open the backdraft

dampers to prevent condensation

from forming water on the backdraft

dampers.

After some review, the inspectors

determined that Design

Change Notice

(DCN) T35568A had been

implemented in September

1995 which

had revised the 953A and

953B normal positions to "open."

The

DCN

stated that the isolation dampers

were to remain open to prevent

moisture accumulation

on the backdraft dampers.

In the past,

condensation

of the

SPE steam

had accumulated

above the dampers

and

degraded

the dampers.

The caution order

0-96-0355 referenced

PER 960695

and Technical

Operability Evaluation

(TOE) 0-96-66-0695 which addressed

the problems

with the backdraft dampers.

The TOE specifically addressed

acceptability of the condition at the time of exceeding

10 standard

cubic feet per minute leakage

on the. backdraft

dampers.

The

TOE was

closed in September

1996 after work was performed

on the dampers

and the

leakage rate was reduced.

Apparently, the caution tag was subsequently

issued to isolate the

SPE bypass,

forcing flow through the main

SPE

discharge line. to address

low flow conditions in the lines.

The

inspectors

did not find any open document directly relating to permanent

resolution of the problem which resulted .in the caution tag.

However,

Work Order 97-000712-000

was open which notes that the dampers

are shut

by the caution order and requests

an inspection of the backdraft

dampers.

The inspectors

noted that the dampers

had remained positioned

differently than configuration control drawings for approximately

one

year.

0

20

The licensee

subsequently

completed

a 10CFR50.59 screening

review and

safety assessment

in accordance

with Site Standard

Practice

SSP-9.4

on

July 24,

1997..

The assessment

concluded. that the alignment was

acceptable

from a nuclear safety viewpoint and did not represent

a

unreviewed safety question.

Work Order 97-000712-000

was rescheduled

to

an earlier date to perform inspections of the backdraft

dampers.

During a subsequent

review, the inspectors

noted that the safety

assessment

included

an incorrect statement.

The assessment

stated that

the situation did not represent

a change to the facility as described

in

the

UFSAR.

This resulted in a safety evaluation not being performed at

the time the assessment

was completed.

'One of the inspectors identified

that the drawing depicting damper configuration and note ll (described

above)

was included in the

FSAR.

On August 13,

1997,

a safety

evaluation

was completed which satisfactorily addressed

the condition.

The inspectors identified that the steam packing exhauster line stack

isolation dampers

had been. positioned differently than configuration

control drawings for approximately

one year to address

an equipment

performance

issue.

There is not

a specific regulatory requirement to

have

a completed safety assessment/evaluation

for such

a condition.

The

inspectors

did not identify any safety concerns with the equipment

aligned in accordance

with the engineer's

instructions

and the caution

tag.

The inspectors

concluded that the primary concern is that actions

were not initiated to address

permanent

resolution of the problem.

The inspector

reviewed the circumstances

surrounding

two instances

of

incorrect oil added to the Unit 1/2 EDGs.

F

The inspector

determined that two separate

aspects of this problem

should be addressed.

The first aspect dealt with the fai lure of the

licensee to promptly identify that zinc additive oil had been put in the

2A EDG.

This fai'lure led to the incorrect oil also being put into the

20

EDG approximately four months later.

The second

aspect of the

problem dealt with the procurement control deficiencies

which permitted

the incor rect oil to be used in both

EDGs.

On February

1,

1997,

Nechanical

Naintenance

(NN) added lubricating oil

to the Unit 1/2A EDG in accordance

with work order

(WO) 97-001076-000.

The

WO documented

work instructions in a step text format which directed

NN to add oil to the

EDG through the oil strainer

box and referenced

TVA

Item Identification Code (TIIC) CAQ-0608.

The inspector

reviewed the

archived copy of the Power Stores

procurement

form (Form 575) and

verified that TIIC CAQ-0608 was procured.

One 55 gallon drum ot oil was

added to the 2A EDG.

On July 2.

1997,

NN added

55 gallons of oi-1 (TIIC

CAQ-0608) to the 20

EDG while performing

WO 97-006843-000.

The licensee

was informed of high zinc content in oil chemistry samples

for the 2A EDG on July 9,

1997,

when

a preliminary copy of the chemistry

report was faxed to the site from TVA Central

Labs.

The report included

data

from several

lube oil samples

for the 2A EDG.

The following five

samples.

taken

on the dates

noted, identified that zinc exceeded

the

vendor limit of 10 ppm maximum:

03/06/97

03/27/97

05/10/97

06/09/97

06/19/97

148

ppm zinc

125 ppm zinc

170 ppm zinc

169

ppm zinc

166 ppm zinc

Subsequent

testing

on July 14.

1997.

revealed that the zinc content in

2D

EDG was

147 ppm.

The concern with zinc in the lube oil is that oil containing zinc

additives could, over

a period of time, result in damage to the

EDG

bearings

which contain silver.

Unit 1/2

EDG A/8/C/0 oil samples

taken

July 14,

1997, indicated

<1 ppm silver, which indicated that no

significant degradation

had occurred.

The licensee

determined that TIIC

CAQ-0608 was not procured

as

a zinc tree oil.

On July 14,

1997, the licensee

drained the lube oil from the "A" EDG and

installed

new filters and oil using work order

(WO) 97-007028-000.

Preliminary test results

from the oil sample taken

on July 14,

1997,

indicated that the zinc levels in the 2A EDG had dropped to ll ppm.

The

licensee

replaced the oil in the

2D

EDG on July 25,

1997.

0

22

The inspector

discussed

the review of the oil chemistry test results

with the component

engineer.

The component

engineer typically reviewed

chemistry reports f'r oil samples after the report arrived at the site.

The review process

did not prompt questioning if expected

sample reports

were excessively

delayed:

The inspector

concluded that weaknesses

in

the licensee's

review of oil analysis

reports permitted the introduction

of the same high zinc oil into a second

EDG.

This issue will remain open pending additional

NRC inspection of the

licensee's

corrective actions to preclude recurrence of the problem.

This item will be identified as Unresolved

Item 50-260/97-08-02,

Incorrect

Oi 1

Used in Two EDGs.

During investigation of the high zinc levels identified by chemistry oil

samples,

the licensee

determined that an error had occurred during the

review and change of TIIC numbers.

TVA Corporate

had evaluated

lubricating oils for generic

use in TVA's nuclear plants.

Apparently.

during the process,

an incorrect generic oil substitute TIIC number was

coded to replace the currently used

EDG oil TIIC number.

This incorrect

oil was placed into two of the

EDGs as discussed

previously.

Another recent procurement

example involved incorrect sized lightbulbs

being used in Appendix

R emergency lights.

The. licensee identified this

issue in BFPER971175.

The inspector

previously identified a concern that ethylene glycol could

have been issued'or

use in the

EDGs contrary to Site Standard

Practice

SSP-13. l. Chemistry Program.

This issue

was described in NRC IR 50-

259.260.296/96-13.

The inspectors

discussed

their concerns

regarding procurement

deficiencies

during

a meeting with licensee

management

on August 5,

1997.

Subsequently,

the inspectors

were briefed on the licensee's

ongoing .initiatives in the Materials/Procurement

area.

The licensee

has

identif'ied numerous

issues with the materials

procurement

processes

at

BFN and at the other nuclear sites.

A team has

been established

which,

in recent weeks,

has finalized an action plan to address

the Materials

issues

and potential actions for improvement.

The inspectors

specifically noted that this Materials Upgrade Project is expected to

address

the

common causes

of the concerns

noted above.

The licensee

intends to address

numerous

other

issues.

For example,

progress

has

been

made regarding

a careful

review and identification of critical

il

23

parts for an important safety system.

The proposed actions include

extensi.ve

data

base revisions

and simplifications to complex processes.

Additional

NRC review of the Materials Upgrade Project is warranted.

These

issues

are identified as Inspection

Followup Item 50-260,296/97-

08-05, Materials Upgrade Project.

Weaknesses

in the licensee's

lubrication oil analysis

program permitted

the incorrect type of lubricating oi-1 to be added to a second

EDG

several

months after it had been installed in a different

EDG.

An error

in the Materials/Procurement

processes

resulted in workers procuring the

incorrect oil for addition to the

EDGs.

Similar examples of procurement

weaknesses

have been identified previously.

The licensee

has initiated

an extensive Materials Upgrade Project to address

the issues.

E2.4

The inspector

reviewed selected

plant modi.fications in order to veri fy

that (1)

10 CFR 50.59 Safety Evaluations

were technically adequate

and

the screening criteria had been correctly applied;

(2) plant

modification packages

identified all plant procedures

that required

revision because of the design changes;

(3) post modification test

scoping

documents

were technically adequate to demonstrate

achievement

of design objectives;

and (4) work instructions adequately

addressed

the

scope of the plant modification and was consistent with the hardware

changes.

Implementation of the design control process

was also verified

to have complied with the requirements of the licensee's

ANSI N45.2. 11-

1974 design control program.

r

i n

The following plant. modifications were reviewed during this inspection:

~

DCN No. T34764A, Replace Obsolete

Melestrom Pressure

Switches with

SOR Pressure

Switches,

Revision 0.

~

DCN No. T39722A. Modify RFW Heater

Isolation Logic, Revision 0.

~

DCN No. W35344A. Replace

APRM/RBM with Power

Range Neutron

Monitors, Revision 0.

Ci

~

DCN No. W36756A,

Upgrade

Scram Solenoid Valves, Revision 2.

~

DCN No. S39677A,

Revise

Load Limitations, Revision 0.

The licensee's

design control program permits the development

and

implementation of various alphabet

designated

plant modifications

as

defined in procedure

SSP-9.3,

Plant Modifications and Design

Change

Control, Revision 22, Section 5.0 Definitions.

Review of the above two

Ts, two Ws and one

S plant modification revealed that in general

the

design

change

packages

were developed

and implemented in accordance

with

the design controls delineated in plant procedure

SSP-9.3.

The

'nspector

considered

the overall design control process to be complex

and cumbersome

because of the various administrative processes

required

for each type of plant modification.

As a typical example plant

procedure

SSP-9.3 defined the

S-DCN as

a type of DCN that is used to

support documentation

changes

only.

An S-DCN shall not be used for

setpoint

changes.

system realignment,

nor labeling changes.

This design

process

was used incorrectly for system alignment changes,

as described

in the following paragraphs.

Based

on review of DCN No. S39677A the inspector

determined that the

scope of the design

change

involved revising load limitation notes

on

drawings

0-45E732-1,

0-45E732-3,

0-45E7349-1,

and 1-45E749-2.

The load

limitation note was revised to permit simultaneous

operation of

transformers

TS1E and

TDE from the 4160 Volt Diesel Generator Auxiliary

Board "B" based

on

a maximum load limit of 500

KVA.

Design basis

calculation

ED-Q0057-950036,

AC and

DC Load Limitations for Units 2 and

3 Operating.

was reviewed

and verified to have established

a load limit

of 500

KVA for this system alignment.

The licensee

revised drawing

numbers

0-45E732-1

and 0-45E732-3 which were

FSAR Figures 8.5-12A and

8.5-13A respectively.

An FSAR change

request

was also prepared

as part

of the

DCN package in order to incorporate the design

changes

into the

licensing basis

document.

The inspector

reviewed the Safety Assessment

performed for plant

modification

DCN No. S39677A and determined that it failed to identify

the need for a Safety Evaluation.

Revision of the load limitation notes

on the

FSAR Figures

changed the technical

content of the Figures in the

FSAR and should have

been evaluated in accordance

with the requirements

of 10 CFR 50.59.

This change permitted

a new system alignment which had

previously been prohibited because of the current licensing basis.

The.

licensee failed to perform

a

10 CFR 50.59 Safety Evaluation because

the

change

was considered

a documentation

change only.

This fai lure to

25

perform

a

10 CFR 50.59 Safety Evaluation for simultaneous

operation

of'ransformers

TSlE and

TDE involving a new system alignment

was

identified as Violation 50-260/97-08-01.. Failure to perform

a

10 CFR 50.59

Safety Evaluation for new system alignment.

The inspector

reviewed the safety assessment/safety

evaluation

prepared

for the other plant modifications in order to verify the technical

adequacy

and compliance with the requirements

of 10 CFR 50.59.

The

safety assessments/safety

evaluations correctly applied the screening

criteria in assessing

the impact of the changes to the plants licensing

basis delineated in the

UFSAR and the Technical Specification.

Additionally, the safety assessments

clearly described

the changes

implemented within the scope of the plant modifications

and concluded

that

an unreviewed safety question did not exist because of the design

changes.

The inspector

concurred with the conclusions

documented.

The licensee's

design controls required that

DCN Impact Review Forms be

completed

by Systems

Engineering,

Operations

and Maintenance for T and

W-DCNs.

Each organization

was responsible

for identifying the

procedures/instructions,

for which they have responsibility, that

required revision prior to:

(1)

Returning the modified equipment/system

to operation

(2)

Final closure of'he

DCN

Plant procedures

or instructions -that are required to maintain the

systems

in a functional/operable

status

were required to be revised

prior to return to operation.

Additionally, procedures

other than those

that are revised prior to return to operation

need to be revised before

closure of the

DCN.

Detail guidance for completing .the Impact Review

Forms

was provided in Appendix

E of SSP-9.3.

The inspector

reviewed

completed

Impact Review Forms for the above plant modifications

and

verified that the requirements

had been satisfied.

One item was identified during this review in connection with DCN

W36756A.

This plant modification was prepared to replace existing

ASCO

scram solenoid pi:lot valves,

scram discharge

valves vent and drain pilot

valves,

and scram discharge

valve isolation test valve with solenoid

valves that had

a longer qualified life.

The Impact Review Form for

this plant modification was verified as having been completed to

initiate revision to procedure

MCI-0-085-HCU001.

The inspector

determined.

that mechanical

corrective instruction MCI-0-085-SOLOOl and

Il

il

26

electrical corrective instruction ECI-0-085-SOL001 which implement

essential

maintenance

requirements for Environmental Qualification

Binder BFNOEQ-SOL-0010 were not listed as requiring revision on the

Impact Review Form.

Discussions with TVA management

revealed that

procedure

MCI-0-085-HCU001 had been replaced

by the two plant procedures

identified above.

Several

changes

in the

ASCO valve model

number's

were

documented in the plant modification package

and these

changes

occurred

in response to industry wide concerns

involving the elastomer

material

used with the valves.

The most recent revision of the

DCN identified

the replacement

SSPVs

as

ASCO model

HV 266000-7J for which plant

procedures

had not yet been identified on the impact review forms.

This

omission appeared to be an anomaly in that the voiding of procedure

MCI-

0-085-HCU001

and its replacement

by other procedures

was not entered

into TVA's document

and records

management

system.

Several

changes

in

ASCO valve model

numbers

and elastomer

types also exacerbated

this

situation.

Problem Evaluation Report

PER No.

BFPER971046

was written to

document this deficiency and initiate corrective action.

The inspector

considered this item to be of'inor safety significance.

The inspector

performed additional

reviews of the plant modification

packages

including work completion statements.

Drawings and design

change authorizations

required for completing the plant modification

including post modification tests

documents

were identitied in the work

completion statements.

Review of selected

post modification test

scoping

documents

revealed that test acceptance criteria were adequate

to demonstrate

achievement of design objective.

No deficiencies

were

identi.fied during this review.

The inspector concluded that the licensee

was implementing the design

control program in accordance

with the requirements of ANSI N45.2. 11-

1974.

One Violation was identified for fai lure to perform

a

10 CFR 50.59 Safety Evaluation during implementation of an "S" DCN.

i

I

v

1

(37550)

The inspector

reviewed selected

Technical Operability Evaluations

(TOEs), in order to evaluate the technical

adequacy of the formal

engineering

input used for aid in determining operability.

The TOEs

were also reviewed to verify compliance with the guidelines of Generic

27

Letter 91-18 for ensuring the functional capability of a system or

component.

TOE No. 0-97-085-0974, Justification for Continued Operation with Scram

Solenoid Valves Containing Incorrect Material

TOE No. 0-97-085-0974,

Revision 0,

was written to provide justification

for continued operation with regard to potential safety related

problem

involving ASCO model

HV 266000-007J

solenoid pilot valves.

The

Automatic Switch Company

(ASCO) in a letter to the

NRC dated

May 27,

1997, provided additional information concerning the potential safety

related problem with ASCO model

HV 266000-007J

scram solenoid pilot

valves

(SSPVs).

In this letter

ASCO identified a total of six plants

that had received the suspect

SSPVs.

Browns Ferry was listed as having

received five.

Corrective actions described in the letter included

a

Justitication for Continued Operation

(JCO) prepared

by the General

Electric Company

and which were distributed to the affected plants.

The

JCO recommended that pre-tested pilot valves assemblies

be installed

on

all suspect

valves before they reach the predicted three to four year

end-of-life.

Additionally. the JCO recommended that augmented air

leakage testing

be considered for the plants until the changeout

can be

completed.

The inspector

reviewed TVA's JCO in order to verify that GE's

recommendations

had been incorporated

and compensatory

actions

were

being taken

for the degraded

SSPVs.

Based

on this review the inspector

determined that four Unit 2 SSPVs would be changed

out at the next

refueling outage

(RFO) scheduled for the end of September

1997.

Similarly, one Unit 3 SSPV would be changed

out at the next

RFO

scheduled f'r September

1998.

TVA concluded that the service life of

the

SSPVs

based

on their installation date

was well within the

GE

recommended life of the elastomers.

Compensatory

actions to be

performed for the Unit 3 SSPV will involve, additional

scram time testing

on a frequency of 16 weeks for control rod 26-31 until replacement of

the pilot head subassembly

per

WR C385168.

The inspector identified no

deficiencies

during review of. TOE No. 097-085-0974.

TOE No. 0-94-086-0169,

0/G "D" Instrument Air Root Valve

TOE No. 0-94-086-0169

was written to evaluate the installation of a non-

safety valve in a safety related

system.

System

086, diesel starting

0

28

air system right bank instrument root valve 0-RTV-086-0602D was

installed by Work Order 91-39183-00

and was requi red to maintain system

pressure for enabling the "D" diesel

generator to start.

The licensee

determined that the .apparent

cause for installation of the non-safety

valve to be an inadequate

procedure in that procedure

SSP-6.2.

Maintenance

Management

System,

did not provide clear guidance

concerning

replacement

parts.

The procedure

paragraph

3.9. 1 was revised

on October

26,

1994, to preclude future occurrence of this issue.

The installation

was accepted

as-is

based

on the valve design

and post installation

tests.

The valve installed

was

a

NUPRO B4J rated at 250 psi at 300

degree fahrenheit.

System design temperature

and pressure

was given as

300 degree fahrenheit

and 200 psi.

The TOE was closed

based

on post

maintenance

tests results which verified no leakage through the seat

and

no visible leakage at the valve with the system in service.

The basis for closing the

TOE did not consider

seismic requirements.

The inspector

considers this to be of'inor safety significance given

the small

mass of the instrument root,valve and the redundancy

designed

into the diesel starting air system.

Additionally. the inspector

considered

the licensee's

corrective actions were adequate to prevent

reoccurrence.

TOE No. 0-94-026-9006,

Fire

Pump Auto Start Circuit

This TOE was written to evaluate the installation of temporary jumpers

on the fire pump auto start ci rcuit while plant modification

DCN No.

W18627A was being implemented.

The plant modification added

redundant

Class

1E fuses for cables

FE100 and A1225 in order to resolve electr ical

separation

concerns of non-safety related circuits degrading safety

related circuits.

Installation of the temporary jumpers provided

electrical

power from 120

VAC preferred

bus

on panel 9-24, breaker

512

to auto start terminal points

WFXl and

WFY1.

The auto start circuit was

therefore enabled while fuses

0-FU2-026-512A and

B were being installed.

This temporary plant modification was implemented

by work plan 0626-93

for which

a

10 CFR 50.59 safety Evaluation

had been

per formed.

No

deficiencies

were identified during review of TOE No. 0-94-026-9006.

TOE No. 2-96-211-9003,

Transformers

TSlE and

TDE Simultaneous

Operation

This

TOE was written to permit paral,lel operation of transformers

TS1E

and

TDE from the 4160

V Shutdown

Board "B" despite specified

restrictions

on approved design output drawings.

The TOE failed to

recognize that

a plant modification should have been

used to implement

0

ik

29

this design change.

Failure of the

TOE to initiate a plant modification

was recognized

by TVA management

and

PER No.

BFPER960512

was written to

initiate

DCN No. S39677A for revising the load limitations notes

on

drawings

number 0-45E732-1,

0-45E732-3,

1-45E749-1,

and 1-45E749-2.

The

DCN is further reviewed in Section E2.4.

The

TOE documented

a technical evaluation for the load limit specified

on the referenced

drawings

and provided quantitative acceptance criteria

of 77 Amps for a load limit of 555 KVA.

The inspector

reviewed design

basis calculation

ED-00057-950036,

Revision

2 and verified that

a load

limit of 500

KVA had been established

as the load restriction for

simultaneous

operation of transformers

TS1E and

TDE.

Based

on the load

limit of 500

KVA the inspector calculated the load current to be 69.3

Amps which was ditf'erent from the value given in the TOE.

The TOE also stated that procedure 0-0I-578,

480/240

VAC Electrical

System,

Revision 53, should be revised to include instructions for

simultaneous

operation of transformers

TS1E and TDE.

The inspector

reviewed the procedure

and verified that the procedure

had been revised

to permit parallel operation of,both transformers

based

on

a load limit

of 500 KVA.

A 10 CFR 50.59 Safety Evaluation

had also been

perf'ormed to

incorporate these

load limit restrictions into revision 48 of the

procedure.

Section 3. 14 delineated

the precautions

and limitations for

parallel operation of the transformers.

Based

on review of the

procedure,

the inspector determined that the procedure did not provide

quantitative acceptance criteria within the body of the procedure

for

parallel operation of transformers

TS1E and

TDE under load limiting

conditions.

Section 8.6 of the procedure delineates

the instructions

for transferring

480

V shutdown board

"1A" from the normal to the

alternate

power supply.

Section 8. 10 provides similar instructions

for

transferring the 480

V diesel auxiliary board

"A" from the normal to the

alternate

power supply.

The procedure did not identify within either

sections

8.6 or 8. 10

a load limiting value of 500

KVA for system

alignment

implemented

by performance of both of these sections.

The

licensee stated that the precaution

and limitation statement

in Section

3. 14 which required calculation of the load current under this mode of

plant operation

was adequate for this plant evolution.

The inspector

considered

the procedure

adequate,

.however,

omission of quantitative

acceptance criteria within the body of the procedure

could result in

human errors.

The Resident

Inspector

observed

implementation of such

an evolution as discussed

in Section 01.2.

0

0

30

The inspector concluded that the TOEs were technically adequate

with

some minor exceptions.

E8

Hiscellaneous

Engineering

Issues

(92903)

E8. 1

1

,

Emergency

Core

Cooling System

(ECCS) Inverter Failures.

This IFI addressed

several

fai lures of the Unit 3

ECCS inverters which have occurred since July

1996.

The cause of the inverter failures

and potential affects of

ambient

room temperatures

were not fully understood.

A total of five

incidents

have occurred

on the Unit '3 inverters, inverter component

replacements

were required in four of'he instances

and in one case

a

fuse cleared.

Inspection Reports

259,260,296/96-08,

96-12,

and 96-13

contain description of NRC review of several of the incidents.

The

licensee

has submitted Licensee

Event Reports

on the failures.

The licensee

performed extensive investigation into the failures

including:

~

The failed Silicon Controlled Rectifiers

(SCRs) were analyzed

by a

vendor

and

an independent testing

company.

The analysis

noted

that the epoxy encapsulant

in the failed SCR did not completely

fill the lower cavity and

an air bubble

may have been present.

The SCR failed at

a corner where it is most susceptible to voltage

stress

and the analysis

concluded that the fai lures were related

to an overvoltage condition.

~

Extensive online monitoring of the inverters

and investigation by

the licensee

ruled out potential

causes

such

as electronic noise,

radio. transmissions,

power supply transfers,

or other plant

evolutions.

Reviews of Operating

Experience

Data indicated that

inverter fai lures which had occurred at other facilities were not

similar. to these failures.

~

A technical

assessment

was .conducted

by a TVA corporate electrical

engineer

and

a representative

of SCI.

The review concluded that

the most likely cause of four of the five failures was

damaged

or

defective

SCRs.

The other failure (fuse clearing) apparently

0

involved a loose air-core inductor which shorted

a capacitor

bus.

The

review stated that the inverter

vendor

has concluded that the inverter

components

are optimized for stable operation for the range of voltage,

loading,

and ambient temperatures.

Corrective actions

implemented included:

125

amp inverter fuses

were replaced with 100

amp fuses

on Unit 3

(and will be replaced

on Unit 2).

The fai led SCRs were Solidstate Controls Incorporated

(SCI)

SCR

type TD 42.

The vendor has replaced

TD 42 SCRs with TD 46 type.

The TO 46 SCRs have larger I't ratings than the

TO 42 SCRs.

A modification

(DCN T39853)

was implemented

on Unit 3 and is

planned

(DCN T39852) for Unit 2 which adds

a 250

VDC to 24

VDC

converter.

This converter will provide an alternate

supply to the

Analog Trip Units if'n inverter failure occurs.

This

significantly reduces

the potential satety affects of an inverter

failure.

IR 96-08 noted that

a

NRC inspector identified that

some of the

inverters did not have the minimum clearance to the wall stated in the

vendor

manual.

The inspector noted that an SCI field service repair

report.

dated February

1997, stated that the inverter temperatures

were

well within limits.

Problem Evaluation Report

(PER) 961123

was

initiated to address this issue.

The inspector

reviewed the completed

PER.

The licensee's

investigation concluded that one of the causes of

the problem was that the vendor instruction manual which contained the

clearance

requirements,

was not supplied

on the front end of the

procurement

process

and thus the information was not incorporated into

the installation design.

The licensee

concluded that the lack ot

clearance

was not

a factor in the recent failures and noted that the

Unit 2 inverters are installed closer to the wall than the Unit 3

inver ters

and have not experienced, the

SCR failures.

The licensee

obtained concurrence

from the vendor that the installed configuration is

acceptable

and incorporated

documentation into the vendor

manual.

The

inspector

reviewed

a memorandum which clearly stated that the vendor did

not feel that the cabinet spacing

was

a problem.

Site Engineering

issued

a

memo to the Procurement

Engineering

Group reinforcing the

obligation to obtain special

design requirements

on the front end of a

contract

and request that such information be addressed

on vendor

drawings

so that it can be incorporated into the design package.

0

0

32

The inspector concluded that the licensee's

overall investigative

and

corrective actions regarding the inverter failures were timely and

effective.

No failures of the replaced

SCRs

have occurred.

The

inverters are being monitored by the licensee

as

an a(1) system in

accordance

with the maintenance

rule.

The failures

and corrective

actions

were well documented

in the licensee's

corrective action system.

IFI 296/96-08-02 is closed.

E8.2

1

, Resolution of FSAR

Discrepancies.

During a review of the Final Safety Analysis Report

Section 4.7.7, the inspector

questioned

the following statement:

"Testing of the RCIC pump discharge

valve and air-operated

check valve

is accomplished

by first shutting the upstream discharge valve."

The

licensee

reviewed the statement

and determined that

a discrepancy

existed

between the

FSAR statement

and the way that the testing is

currently conducted.

The licensee initiated BFPER971070

on July 8,

1997.

The IFI remains

open pending additional

NRC review of the

licensee's

UFSAR review program.

f8.3

Torus Water, Level

Exceeded

Technical Specification

(TS) Limit Due to a Past

Engineering

Error.

This

LER addressed

the licensee's

identification that

a 2 inch

offset in the narrow torus water level instrumentation

had resulted in

torus level slightly exceeding the -1 inch TS limit in the past.

This

issue

was reviewed in detail

by NRC inspectors

as documented in IR 95-

64.

Non-Cited Violation 95-64-09, Violation of Torus Water Level TS,

addressed

the deficiency.

The

LER is closed.

E8.4

n

, Failure of the High

Pressure

Coolant Injection Steam Supply Valve During Testing.

The

licensee

determined that pitted seal-in contacts

in the steam supply

circuitry caused

the. problem.

IR 95-31 describes

NRC review immediately

following the failure.

The inspector

reviewed closed

PER 950690

and

maintenance

work records.

The documentation

indicated that the valve

was stroked

on September

8.

1995.

(which verified the contacts

were

operating)

and the contacts

were inspected

on December

1,

1995.

Work

Order 95-14730-00 stated that the contacts

were found in good condition.

The inspector also verified that procedure

EPI-0-000-MCC001 is scheduled

to be performed

on the breaker during the upcoming refueling outage.

No

other

problems with these contacts

have occurred'since

the 1995 failure.

The

LER is closed.

0

0

0

E8.5

33

In April of 1996 TVA's Vendor Audit Services

received information from

NUPIC concerning continuing weaknesses

in Ellis and Watts commercial

grade dedication

processes

and this vendor was

removed from the Accepted

Supplier List (ASL).

Vendor surveillance

report number 96S-18,

dated

June

17,

1996,

documented

TVA's evaluation of commercial

grade

dedication

packages

for several

Browns Ferry purchase

orders.

The

vendor surveillance

was performed at Ellis and Watts, Batavi a,

Ohio on

May 9-10.

1996.

The inspector conducted

interviews with TVA's personnel

from.the Procurement

Engineering

Group

(PEG)

and reviewed objective

evidence which provided reasonable.

assurance

that material

accepted

from

Ellis and Watts, had met specified technical

and quality requirements.

The fol,lowing documents

the results of this review:

Purchase

Order

(PO) 96N2D-156126

was issued

for two Spartan

solenoid

valves which had not yet been shipped at the time of the evaluation.

This contract

was canceled

and the material

was never received

from the

vendor.

PO 96N2R-167653

was .issued for ten Spartan

solenoid valves.

TVA

approved Ellis and Watts revised

commercial

grade dedication plan

CDPN-

0723 on May 10,

1996.

Critical characteristics

had been verified by a

combination of inspection

and commercial

grade survey.

Additionally, a

sample of these valves were examined

and no deficiencies

were

identified.

The material

was received

and accepted

from the vendor.

PO 95N2R-171612

was issued for two solenoid valves; this material

was

processed

and received prior to the vendor being

removed from the ASL.

Commercial dedication plan CDPN-0729 was approved

by TVA and critical

characteristics

were verified by a combination of inspection

and

commercial

grade survey.

The package

was determined to be acceptable.

PO 95N2R-149040

was issued for two Metrex chiller valves.

Commercial

dedication plan CDPN-0702 was reviewed

and approved

by TVA with the

following exceptions:

~

Verification of material for pressure

boundary items was not

validated

by the vendor.

0

0

0

34

~

Hydro test pressure

values

documented

in the

CDPN and the actual

test results

were different.

The

CDPN showed test pressure of 280

psig and the test report specified. Z25 psig.

Additionally.

PO 96NZR-16556 issued for three Hetrex chiller valves

was

determined to be satisfactory

based

on review of dedication plan

CDPN-

0719 with an exception similar to the first one identified above.

The

exceptions

were resolved via correspondence

with the vendor and material

tests

performed

by TVA's Central Laboratory Services.

The chemical

composition of the valve material

was identified in Centra1

Laboratory

Services

Technical

Report

No. 96-1098,

dated July 8.

1996.

PO 96N2R-166372

was issued

for one crank case heater

and its commercial

grade dedication plan CDPN-0720 was reviewed

and .approved

by TVA.

An

examination of the heater revealed.

however, that it differed from the

sketch provided by the vendor with regard to the length of the leads

required for power connection.

The two heaters

also differed in

appearance.

Based

on the results of TVA's investigation of this issue

one heater

was determined to be acceptable

for shipment

and the other

was not released for shipment

pending the vendor

making an equivalency

determination for the other.

The inspector concluded that the actions taken by TVA for release of

material

received

from Ellis and Watts was adequate to ensure that

technical

and quality requirements

involving critical characteristics

of

procured items were satisfactory.

E8.6

1

This violation identified that

on February

2 and 4,

1993, the licensee failed to ensure that the

provisions of 10 CFR 50.7 were implemented in that Stone

and Webster

Engineering Corporation,

a contractor to the Tennessee

Valley Authority

at the Browns Ferry Nuclear Plant, discriminated against

a worker

engaged

in a protected activities.

Specific corrective action for this violation was reviewed

and

documented

in NRC Inspection Report 50-260,

296/96-13.

This violation

is closed for record purposes;

however. the staff will continue to

monitor plant specific indicators related to discriminatory employment

practices.

These indicators include, in part, allegations of

discrimination reported to the

NRC and proceedings initiated as

a result

of complaints

made to the Department of Labor alleging discrimination

0

0

35

practices.

These indicators include. in part. allegations of

discrimination reported to the

NRC and proceedings initiated as

a result

of complaints

made to the Department of Labor alleging discrimination

for engaging in protected activity.

R4

Staff Knowledge and Performance

in Radiological Controls

and Chemistry

R4.1.

The inspector

observed

sampling ot the

Raw Cooling Water

(RCW) system.

In accordance

with Inspection Procedure 71750,

compliance with

procedural

and Offsite Dose Calculation Manual

(ODCM) requirements

was

examined.

b.

II

On July 17,

1997,

one of the inspectors

observed

sampling of the Unit 1

RCW system.

The sampling

and analysis

was being conducted

because

the

Unit 1

RCW effluent radiation monitor (RM-90-132D) was inoperable.

Table

1. 1-1 of the

ODCM (Action D) requires

sampling at least

once every eight

hours during

RCW releases

.when the monitor is inoperable.

The monitor

had been inoperable since July 4,

1997.

The inspector

observed that the

licensee

had good administrative

methods to ensure that the sampling

was

performed within the required intervals'nce

per six hour sampling

requirements

were actively tracked

by the Chemistry Shift Supervisors

and turned over between the Radiological Laboratory Assistants

(RLAs).

The data

package

for completion of the procedure

contained signatures

for verification that the time requirements

were met for each

sample.

The sampling

and analysis is controlled by Surveillance Instruction 0-

SI-4.2.D-3B,

RCW Effluent Radiation Monitor (Off-Line) Inoperable,

and

Chemistry Instruction (CI)-403, Reactor Building Sampling Procedure.

The

RLA notified the Unit 1 Operator

and reviewed the surveillance

requirements prior to obtaining the sample.

However, the

RLA did not

perform several

steps in accordance

with the procedure.

Step 7.7 of O-SI-4.2.D-3B states that the sample

volume is to be

collected for gamma

scan

per Attachment

15 of CI-403.

Step 1.2 of CI-

0

36

403 required that valve 1-24-880 be verified open.

This valve is

a

small

manual isolation valve between the

RCW outlet line and the sample

pump.

The RLA failed to verify that the, valve was open.

Step 1.3 of CI-403 required the worker to check the operating status of

the sample

pump.

Sampling is performed differently depending

on sample

pump status.

The step contained specific directions that the sample

pump is operating if the

"MOTOR ON" light on Panel

25-336 is

illuminated.

The sample

pump is not operating it the

"MOTOR OFF" light

is illuminated or if all Panel

25-366 lights are extinguished.

All the

lights were extinguished.

(The error in panel

numbers

had been

previously identified and was being addressed).

In response to the

inspector's

questions.

the worker discussed

that he had verified that

the

pump was operating

by direct observation of the pump and sample tlow

indication on the panel

instead of the procedural

requirements.

The

inspector observed that the sample

pump appeared to be running and there

was sample flow indicated.

Subsequently, it was determined that the

"MOTOR ON" light bulb had burned out.

The remaining steps

were performed

as required.

The RLA also contacted

Operations

and requested

independent verification that the sample valve

had been shut.

Required information was entered

on the data sheets

for

O-SI-4.2.D-3B and

a

gamma

scan

was performed.

The printout of the

gamma

scan

was forwarded to the Chemistry Shift Supervisor

(CSS) f'r review.

Steps

7. 10-7.12 of the SI require the

CSS to review the data

and verify

acceptance criteria were met.

The printout listed minimum detectable

activity (MDA) in microcuries per milliliter for different isotopes in

the sample

and stated that no activity had been identified in the

sample.

The inspector

asked the

CSS

how he verified the acceptance

criteria that the Lower Limit of Detection

(LLD) of the analysis

was

less than the Effluent Concentration Limit (ECL) (total) .as described in

step 7.9.3 of the SI.

The

CSS responded that he was not sure

how to do

that from the data

on the printout.

Subsequently,

Chemistry department

supervision

informed the inspector that the counting equipment in the

lab .was set

up to meet the requirements

for Lower Limit of Detection.

This was accomplished

by setting

a conservative

minimum count time

period into the routine used

by the

RLAs to count the samples.

The inspector

noted two minor administrative errors in the procedure.

Attachment

2 of O-SI-4.2.D-3B (page

9 of 9) contained

an incorrect title

line and referenced

the Residual

Heat Removal Service Water radiation

monitor.

The inspector

was subsequently

informed that this error

had

been detected

the previous

week and was being corrected.

Step 1.3 of

0

4l

37

the SI contained

an incorrect panel

reference

number.

The inspector

was

informed that Chemistry personnel

had recently identified that error as

well and would correct it.

Browns Ferry Technical Specification (TS) 6.8. 1. l.i requires that

written procedures

shall 'be established.

implemented,

and maintained

covering the activities referenced

in the

ODCM.

Table 1. 1-1 of the

ODCM

states that releases

of'CW may continue, with the number of radiation

monitoring instrumentation

channels

less than the required

minimum.

provided that

a temporary monitor is installed or at least

once

per

eight hours grab samples

are collected

and analyzed for radioactivity.

The worker did not correctly implement written procedure

CI-403 which is

utilized to accomplish the

ODCM requirements.

This failure constitutes

a violation of minor significance

and is being treated

as

a Non-Cited

Violation, consistent with Section

IV of the Enforcement Policy.

The

violation had no actual

impact on the validity of the raw cooling water

sample.

This is addressed

as Non-Cited Violation 259/97-08-04,

Failure

to Follow Chemistry Sampling Procedure.

The licensee

had strong administrative controls in place to minimize the

possibility of missing

a 'ODCM required compensatory

RCW sample.

The

CSS

indicated to the inspector that he was not aware of how the LLD

acceptance criteria (stated in ODCM and the procedure)

was met, although

it was his responsibility to verify that the criteria was met.

The

worker did not fully comply with the sampling procedure.

The safety

significance of the specific deficiencies

was small since the overall

intent of the steps

was met.

However, considering that Chemistry

department

management

has

been emphasizing

procedural

compliance in

recent

months,

the inspector

concluded that the deficiency should be

addressed

by the licensee.

The inspector

noted indications that

management

has also initiated efforts to improve Chemistry, procedures.

R8

Miscellaneous Radiological Protection

and Chemistry Issues

R8.1

v

In accordance

with the guidance in Inspection

Procedure

71707, the

inspector

per formed

a review of the licensee's

10 CFR 19 required

postings at selected bulletin boards

around the site.

0

38

On June 25,

1997, the inspector

noted that an outdated

NRC Form 3 was

posted

on

a bulletin board at the East Gatehouse

protected

area entry

point.

The inspector brought this to the attention of the Site

Licensing Supervisor

and 'a problem evaluation report

(PER)

BFPER971039

was initiated.

In addition,

a current copy of Form 3 was temporarily

placed over the outdated version which was in a locked case

and could

not immediately be removed.

Subsequently,

the licensee

informed the

inspector that the board was not the licensee's

required board,

but was

maintained

by a contractor.

The

NRC Form 3 was

removed from the board.

The inspector also noted'hat

an old version of 10 CFR Part 19 was

posted.

The inspector discussed

with the licensee

how the required

postings

were maintained.

The licensee indicated that they perform

a

periodic review of the posted

documents at seven locations

around the

plant.

The most recent

review was performed

on June 5,

1997.

The

licensee

addressed

the outdated version of 10 CFR Part 19 by adding

an

item to the per iodic review checklist to replace

10 CFR 19.

21 from the

NRC Rules

and Regulations.

On July 11,

1997, the inspector

sampled four of the seven places that

the licensee displays

10 CFR 19 required postings.

The East

and West

Gatehouse

boards

included the

NRC Form 3, Part 19. Part 21.

and

a

licensee

Notice to Employees

which discusses

required postings

and where

they can be viewed.

The remaining two boards

sampled

included the

NRC

Form 3 and the licensee

Notice to Employees.

The inspectors

questioned

the clarity of some of the items in the Notice

to Employees.

On July 17,

1997. the inspector discussed

changes

made 'by

the licensee to the Notice to Employees.

The licensee clarified the

contacts for assistance

in reviewing required documents.

In addition,

the licensee clarified the posting to more accurately reflect the

NRC

position on identity protection of individuals that present thei r

concerns to the

NRC.

The inspectors

considered that the licensee's

actions

were acceptable.

l

F l

Review of

Licensee

FSAR Commitments for

CANs associated

with Units

1 and 3.

Review of this item was documented in Inspection Report 96-06 but due to

an administrative oversight the item was not closed out.

The review was

sufficient to close out the item. the IFI is closed.

0

e

39

Pl

Conduct of Emergency Preparedness

Activities

P1.1

The inspector observed portions of the emergency

preparedness

training

drill which was administered

on July 30.

1997.

The inspector

observed

the drill from the Technical Support Center

(TSC).

The drill appeared to be

a good training opportunity for

participants.

The participants in the TSC provided recommendations

for

improvements

during the post drill critique.

P8

Hiscellaneous

Security and Safeguards

Issues

P8.1

, Failure to Adequately

Control Unattended

Vehicles Within the Protected

Area.

The inspectors

reviewed the licensee's

corrective actions which included

a notice to

vehicle drivers entering the protected

area,

a Site Security memorandum

which directed patrols to increase

checks

and searches

of designated

vehicles within the protected

area,

and training of Facilities and

Instrument

and Controls personnel.

In addition, the licensee

addressed

control of vehicles within the protected

area in the Plan of the Day

Report dated September

23,

1996.

The inspectors

sampled vehicles to

ensure that the vehicles were controlled.

This item is closed.

P8

Hiscellaneous

EP Issues

P8.2

r

Dose Assessment

capability. This item was opened to evaluate whether,

in the event of an

emergency at Browns Ferry,

methods were in place for on-shift personnel

to perform basic offsite dose calculations

using real time

meteorological

data.

Subsequent

detailed in-office review of the licensee's

Emergency

Plan

determined that the licensee

had not committed to have on-shift dose

assessment

capability.

Subsequently,

the licensee

revised

Emergency

Plan to provide for on-shift dose

assessment

capability and revised

their Emergency

Plan, Implementing Procedure

EPIP 14, Radiological

Control Procedures",

Revision 11, to provide that capability.

il~

40

The licensee's

submitted

change to Emergency

Plan Implementing

Procedures

(EPIP)

14, Radiological Control Procedures,

Revision 12,

deleted Section 3.9 f'rom EPIP 14, Revision

11. Section 3.9 had

instructed on-shift personnel

to run Forecast

Radiological

Emergency

Dose

(FRED) to make emergency classifications

in the event of a

radiological release.

FRED was the licensee's

dose assessment

computer

located in the Technical

Support Center

(TSC).

Other changes

in EPIP 14, Revision 12,

enhanced

the manual

method for

offsite dose calculation by adding two tables with multiplication

factors,

one for

a stack release,

and one for a building or ground

release.

The multiplication factors were selected,

based

upon wind

speed

and stability class for distance of 1 mile,

5 miles,

and

10 miles

from the plant.

To determine the dose rate, the radiological release

rate was multiplied by these multiplication factors.

The inspectors

worked through the procedure without any difficulty. EPIP 14. Revision

12 was of sufficient detail to permit on-shift personnel to perform

a

basic dose calculation at given distances

for the plant using real time

meteorological

data.

Exit Meeting Summary

The resident inspectors

presented

inspection findings and results to

licensee

management

on August 5,

1997.

Other meetings to discuss

report

issues

were conducted during the report period.

A formal meeting with

plant management

was also conducted

on July 11,

1997.

During the July

11,

1997, meeting,

the licensee indicated that additional discussion

was

appropriate

regarding two findings in the engineering

areas.

A

subsequent

telephone call with NRC Region II (RII) management

and

a

reactor engineer

from the RII staff, reviewed the licensee's

position on

the two findings.

A subsequent

exit meeting

was conducted

on August 20,

1997, after

additional information was available regarding the High Pressure

Coolant

-Injection system problem, the Standby

Gas Treatment

System testing

items,

and the engineering

review issues.

The licensee

acknowledged

the

findings presented.

Proprietary information is not included in this

inspection report.

II

1

T. Abney, Licensing Manager

J. Brazell, Site Security Manager

R.

Coleman. Acting Radiological Control'anager

J.

Corey, Radiological Controls

and .Chemistry Manager

T. Cornelius.

Emergency

Preparedness

and Planning.

C. Crane, Site Vice President,

Browns Ferry

R. Greenman,

Training Manager

J.

Johnson,

Site Quality Assurance

Manager

R. Jones,

Assistant Plant Manager

S.

Kane, Acting Site Licensing Supervisor

G. Little, Acting Operations

Manager

K..Singer, Plant Manager

J. Schlessel,

Acting Maintenance

Manager

H. Williams. Site Engineering

Manager

IP 37550:

IP 37551:

IP 40500:

IP 62707:

IP 61726:

IP 71707:

IP 71750:

IP 73756:

IP 81502:

IP 92901:

IP 92902:

IP 92903:

IP 93702:

Engineering

Onsi te Engineering

Licensee Self-Assessments

Maintenance Observations

Survei 1'lance Observations

Plant Operations

Plant Support Activities

Inser vice Testing of Pumps

and Valves

Fitness

For Duty Program

Followup-Plant Operations

Followup-Maintenance

Fol,lowup-Engineering

Prompt Onsite

Response to Events at Operating

Power Reactors

. ~

0

VIO

50-260/97-08-01

URI

260/97-08-02

NCV

260/97-08-03

NCV

259/97-08-04

IFI

260,296/97-08-05

Open

Open

Closed

Closed

Open

Failure to perform

a

10 CFR 50.59

Safety Evaluation for

New System

Alignment (Section E2.4)

Incorrect Oil Used in Two EDGs

(Section

E2.3)

Failure to Identi fy Water'ntrusion

into HPCI System Junction

Box

(Section

E2.1)

Failure to Follow Chemistry Sampling

Procedure

(Section

R4. 1')

Materials

Upgrade Project (Section

M8.4 and E2.3)

IFI

259,260,296/97-01-01

Open

Resolution of FSAR Discrepancies

(Section E8.2)

Q.Q5K

LER 296/95-008

Closed

Core Thermal

Power

Exceeded

Operating License's

Maximum Power

Level

Due to a Drifting Temperature

Transmitter

(Section 08. 1)

VIO

296/95-64-01

Closed

Fire Protection

Program

Equipment

Inoperable Without Compensatory

Actions (Section 08.2)

VIO

260/96-03-01

Closed,

Failure to Fol,low Procedures

During

Core Spray Valve Maintenance

(Section

MB. 1)

0

VIO

260/96-04-01

Closed

Licensee Identified Appendix

R

Deficiencies

(Section M8.2)

VIO

259,260,296/EA

.95 220

Closed

Violation of 10 CFR 50.7

(Section

E8.6)

LER 260/96-001-00

Closed

10 CFR Part 50 Appendix

R

Noncompliance Results in the Plant

Being Outside Its Design Basis

and

Being in a Condition Not Covered by

Plant Operating Instructions

(Section M8.3)

'URI

259,260,296/96-13-02

Closed

Toolpouch Issues

(Section M8.4)

IFI

.296/96-08-02

LER

Z60/95-009

LER 260/95-005

. IFI

259.296/95-55.-01

Closed

Closed

Closed

Closed

Emergency

Core Cooling System

(ECCS)

Inverter Failures

(Section

EB. 1)

Torus Water Level

Exceeded

Technical

Specifications

(TS) Limit Due to a

Past Engineering

Error

(Section

E8.3)

Failure of the High Pressure

Coolant

Injection System Supply Valve During

Testing (Section E8.4)

Review of Licensee

FSAR Commitments

for CAMs Associated with Units

1

8 3

(Section R8.2)

VIO

259.260,296/96-10-01

'losed

'ailure to Adequately Control

Unattended

Vehicles Within the

Protected

Area (Section P8.1)

URI

50-260,296/96-05-04

Closed

On-shift Dose Assessment

capability.

pending -additional

NRC review

(Section P8.2).

t

!

i

0