ML18039A253

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Insp Repts 50-259/97-12,50-260/97-12 & 50-296/97-12 on 971207-980117.Violations Noted.Major Areas Inspected: Licensee Operations,Engineering,Maint & Plant Support
ML18039A253
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 02/12/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18039A251 List:
References
50-259-97-12, 50-260-97-12, 50-296-97-12, NUDOCS 9803040159
Download: ML18039A253 (68)


See also: IR 05000259/1997012

Text

U.S.

NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

License

Nos:

50-259,

50-260,

50-296

DPR-33,

DPR-52,

DPR-68

Report Nos:

50-259/97-12,

50-260/97-12,

50-296/97-12

Licensee:

Tennessee

Valley Authority

Facility:

Browns Ferry Nuclear Plant, Units 1, 2,

8 3

Location:

Corner of Shaw and Browns Ferry Roads

Athens,

AL

35611

Dates:

December

7.

1997 - January

17.

1998

Inspectors:

L. Wert, Senior Resident

Inspector

J. Starefos,

Resident

Inspector

E. DiPaolo, Resident

Inspector

W. Bearden,. Reactor

Inspector

(Sections Ml.3. M3)

R.

Chou,

Reactor

Inspector

(Sections

M1.3,

M3)

E. Guthrie, Resident

Inspector,

Brunswick

(Sections

01.2, 01.3.

M1.1)

G. Salyers,

Emergency

Preparedness

Inspector

(Section P2.1,

P2.2,

P3. 1,

P5. 1, P5.2,

P7. 1,

P7.2)

E. Testa.

Health Physics

Inspector

(Sections Rl.1, R2.1,

R2.2)

D. Thompson,

Security Inspector

(Section S1.2)

Approved by:

M. Lesser,

Chief

Reactor Projects

Branch

6

Division of Reactor Projects

Enclosure

2

9'803040159

9202'f2

PDR

ADQCK 05000259

6

PDR

EXECUTIVE SUMMARY

Browns Ferry Nuclear

Plant, Units 1. 2,

8 3

NRC Inspection

Repor t 50-259/97-12.

50-260/97-12,

50-296/97-12

This integrated inspection included aspects

of licensee operations.

engineering,

maintenance,

and plant support.

The report covers

a six-week

period of resident inspection

and inspection in the areas of Maintenance

and

Plant Support by Region II Division of Reactor

Safety inspectors.

o~ei

Control of important plant equipment

and systems

during the diesel

generator

outage for the

12 year

maintenance

inspection

was good.

The electrical

portion of.the

3C diesel

generator

tagout conser vatively used

redundant

means

to ensure

equipment

was de-energized.

One exception to normal site practices

was identified associated

with tagging of removed potential transformer fuses.

(Section 01.1)

Deficiencies were identified during testing of the Reactor

Core Isolation

Cooling system:

~

Poor attention to detai 1 during

a valve stroke test was identified by

the inspector.

The operator

did not closely read

a procedure

step

and

consequently

misunderstood

the actions

necessary

after

a valve stroke

time was determined to be outside the normal

range.

(Section 01.2)

~

The briefing before

a rated flow test

was not thorough in that it did

not include an overview of the test

and did not address

specific actions

of personnel

involved in the test.

. The operator initially established

a

pump flowrate and due to indicated fluxuations, it was not clear to

the inspector

that the specified

minimum value was met.

This was later

corrected.

(Section 01.3)

The licensee effectively monitored control

room deficiencies.

Aggressive

goals

have been set to reduce the number of control

room deficiencies.

Backup

Control

Panel deficiencies

are not included in the control

room deficiency

list although their importance

may warrant increased

awareness.

(Section 02.2)

A licensee identified and corrected non-cited violation was identified

,involving control rod drive temperature

recorders

in the control

room.

Inadequate

procedural

guidance resulted in some of the alarm points being

inadvertently turned off. (Non-Cited Violation 260/97-12-01,

Inadequate

Procedural

Controls

on

CRD Temperature

Alarms, Section 08.1)

Maintenance:

Calibration of the residual

heat

removal

Loop A discharge

pressure

instrument

was performed satisfactorily

and good worker practices

were used during the

surveillance.

Test equipment

was observed to not have foreign material

exclusion protection.

(Section Ml.l)

Good preparation

and detailed planning for the

12 year maintenance

inspection

on the

3C emergency diesel

generator

was evident.

The training of contract

workers using

a surplus diesel

generator

in the training center

was

a good

initiative.

Minor issues

were identified with the control of contr act workers

from a security aspect

(Section M1.2).

A violation of regulatory requi rements

was identified regarding failure to

'romptly

document

a condition adverse to quality identified by the

NRC.

Previous inspections

have identified other

examples

where the initiation of

problem reports

was prompted

by the

NRC.

(Violation 296/97-12-02,

Failure to

Document Condition Adverse to Quality. Section

M1.2)

Setpoint values

used in the instrument calibration

and functional tests

were

consistent with the allowable values

from the licensee's

setpoint

and scaling

documents

and the Technical Specifications

(Section M1.3).

Completed

Work Order

(WO) packages

reviewed by the inspectors

were generally

adequate.

They

contained sufficient details,

work instructions,

and

requirements

for craftworker implementation.

The work. tests.

and

documentation

completed

met the stated

requirements

(Section

M3. 1).

A licensee identified and corrected non-cited violation was identified for one

example of an inadequate

post- modification test associated

with the Unit 3

Drywell Leak Detection System Outboard Return Isolation Valve (Section H3.2).

Improvement

was noted in the post maintenance testing planning process for

recently completed

maintenance

work activities (Section M3.2).

The licensee's

program for controlling temporary modifications was adequate

(Section H3.3).

Overall, the maintenance

department's

self assessment

program was effective in

that management

has identified and pursued

areas

needing

improvement (Section

H7.1):

Numerous maintenance

proficiency indicators are monitored closely for

detection of areas

needing

improvement.

High expectations

are

established

through the establishment

of challenging goals.

Performance

data

from completed observation checklists is effectively

incorporated into monthly reports.

Implementation of the self

assessment

program was prudently revised

by maintenance

management to

focus

on recognized

weak areas.

Some of the observation checklists

were noted

as not sufficiently

critical during self assessments.

The procedural

guidance for the

administration

of the self assessment

checklists

does not accurately

reflect actual

implementation.

Maintenance

management's

expectations

for feedback to the observed individual, signatures

on completed

checklists.

and degree of self-critism were not being met.

A licensee identified and corrected non-cited violation was identified

involving an inadvertent

engineered

safety feature actuation during post

modification testing.

(NCV 50-260/97-12-03,

Inadequate

Procedure

for

PMT.

Section

M8.1)

En ineerin

The licensee

has

implemented significant modifications to increase

the air

system capacity

and reliability.

Insufficient preventive maintenance

on the

control air dryers resulted in several

recent air system transients.

Problems

with the installation of water trap drain lines has resulted in an operator

work around which the licensee is continuing to resolve.

The licensee

has

adequate

measures

in place to periodically verify control/instrument air

quality.

(Section El. 1)

A licensee identified and corrected non-cited violation was identified

involving different residual

heat

removal service water

pump operability

requirements

in Technical Specifications

and the Updated Final Safety Analysis

Report.

The licensee's

safety assessment

provided in the Licensee

Event

Report was thorough.

(NCV 259,260,296/97-12-04,

Design Basis

Not Translated

Properly for RHRSW Pump Requirements.

Section

E8.1)

The Emergency

Preparedness

program overall continued to be strong.

(Section

P3.1)

The

NRC and licensee

goal for declaration of an emergency classification

within 15 minutes of event recognition was exceeded

by 12 minutes during the

loss of station

power event

on March 5.

1997.

It was not clear to the

inspector that the licensee's

evaluation of this aspect

was self-critical and

that the delay was sufficiently explained.

(Section

P3. 1)

Emergency

Response facilities were satisfactorily maintained.

(Section

P2. 1)

Emergency

Preparedness

audits were organized .and objective and satisfied

requirements of 10 CFR 50.54t (Section

P7. 1)

The licensee

had effectively implemented

a program for shipping radioactive

materials required by NRC and

DOT regulations.

(Section Rl. 1)

Radiological conditions in radioactive waste storage

areas

were observed to be

good.

Material was labeled appropriately,

and areas

were properly posted.

(Section R2.1)

RADCON problem reports

were aggressively

evaluated.

cause analysis

performed

and corrective measures

to prevent recurrence instituted.

(Section

R2.1)

Liquid effluent releases

reviewed during this inspection were found to meet

the regulatory requirements

and the compensatory

analysis permitted by the

Offsite Dose Calculation

Manual during the effluent radiation monitor 0-RM-130

outage were satisfactory.

(Section R2.2)

The inspectors

determined that the licensee

had established

in their

procedures

an appeals

process

and

an adjudication process to ensure that

personnel

who were granted

unescorted

access

were trustworthy, reliable and do

not constitute

an unreasonable

risk to the health

and safety of the public.

(Section S1.2)

Summar

of Plant Status

Re ort Details

Unit 1 remained in a long-term lay-up condition with the reactor defueled.

Unit 2 operated at or near full,power with the exception of routine testing

and scheduled

maintenance

downpowers.

Unit 3 operated at or near full power with the exception of routine testing

and scheduled

maintenance

downpowers.

On December

24.

1997. Unit 3 reduced

power

for about

one hour due to a leak on

a Reactor

Water Cleanup

(RWCU) heat

exchanger

flange.

The leak was subsequently

repaired.

At the close of the

report period, the licensee

was pursuing

a more permanent

repair.

While performing the inspections

discussed

in this report. the inspectors

reviewed the applicable portions of the Updated final Safety Analysis Report

(UFSAR) that related to most of the areas

inspected.

No discrepancies

were

identified.

IIOI ll

Ol

Conduct of Operations

01.1

3C Diesel Generator

Removal

from Service

a.

Ins ection Sco

e

71707

The resident inspectors

reviewed activities associated

with removing the

3C emergency diesel

generator

(EDG) from service for the

12 year

maintenance

inspection.

One of the resident

inspector s performed

a

detailed review of the electrical portions of the

3C diesel

generator

tagout.

Another inspector

reviewed licensee

actions taken to ensure

compliance with Technical Specifications

and Operations

Standing Order

OS-0128.

The inspector also reviewed the Probabilistic Safety

Assessment

(PSA) Profile that was developed for the

3C diesel

12-year

maintenance

outage.

b.

Observations

and Findin s

The hold order clearance

used for the

3C DG.outage

was broken into four

separate

tagout groups.

These were electrical.

lube oil and fuel oil,

cooling and instrumentation,

and air starting system.

The inspector

performed

a detailed

check of the electrical portions ot the tagout.

The inspector

reviewed reference

drawings to ensure that protection to

plant equipment

and personnel

was provided by the tagout.

The

electrical portions were adequate.

Redundant

methods of deenergizing

equipment

was used.

For example.

the

DG output breaker

was racked out

and tagged

and also the breaker

control

power fuses

were pulled.

The

inspector

found that the electrical tagout also contained

items that

would prevent engine rotation although this was not necessary

for

electrical protection.

For

example.

the electrical

system tagout

contained tags

on air start system

components to ensure that the engine

was not inadvertently rotated.

The inspector performed

a walkdown of all installed electrical

component

tags.

All components

were in the required positions with the

appropriate

tags in place.

The inspector identified

a minor discrepancy

involving the

3C

DG output breaker

(Breaker

1832) potential transformer

fuses

(3-FU4-3ECAR).

Normally, clearances

on fused circuits (other than

control circuits) have the hold notice tag attached to the fuse

compartment

door after the fuses

have

been

removed from the circuit.

In

this case,

the fuses were removed

and placed in a bag with the tag and

placed

on top of the cabinet.

The licensee initiated

a

PER to

investigate the discrepancy.

The licensee

also performed

a review of

all current

hold orders tags

on non control

power

fuses.

No additional

discrepancies

were noted.

The inspectors verified that the licensee

adequately

implemented the new

license requirements

established

when the Technical Specifications

were

revised for the 12 year diesel

generator

inspection.

The licensee

posted

magenta

operator information cards

and placards for protected

equipment.

On January

11.

1998, the inspectors

reviewed Operations

,Standing

Order OS-0128,

Diesel

Generator

12-Year Outage

Requirements,

Attachment

3C,

3EC

DG Protected

Equipment Requirements.

The inspectors

verified a sample of the attachment to ensure that the magenta

operator

information cards

and placards

were placed

on identified plant

equipment.

The attachment

also specified seven switchyard entrance

placards,

however specific locations were not detailed.

The inspectors

walked down the transformer

yard fence

and noted placards

were placed

on

only two gate entrances.

The inspector questioned

the Shift Manager

(SM) about the locations of the placards.

Subsequently,

the standing

order

was changed to specifically identify the location of 15 placards

to be placed

around the transformer yard, switchyard,

and 161-kV

capacitor

bank.

The inspectors

toured the control

rooms to ensure that

work was not being performed that would make systems

inoperable which

were'equired

during the diesel

generator

outage.

No problems were

identified.

The inspector

reviewed the Probabilistic Safety Assessment

(PSA) profile

and compared it to the SSP-7.1

Dual Unit Maintenance Matrix.

No

problems were found with the profile as

compared to the matrix.

While

reviewing the matrix, the inspector

requested

a copy of the Dual Unit

Maintenance Matrix from the planning supervisor.

The copy that was

provided

(marked

as the current revision)

was

a slightly different

.version of the matrix .than the matrix in the current

SSP-7. 1.

Subsequently,

the licensee

found that the Unit 2 control

room also had

an incorrect revision of the Dual Unit Maintenance Matrix.

The licensee

initiated

PER 980052 to address

the apparent controlled document issues.

0

01.2

, b.

Conclusion

The electrical portion of the

3C

DG system tagout conservatively

used

redundant

means to ensure

equipment

was de-energized.

One exception to

normal site practices

was found with the handling,of removed fuses

and

tags associated

with potential transformer fuses.

Control of important

plant equipment

and systems

during the diesel

generator

outage

was good

Reactor

Core Isolation Coolin

RCIC

S stem Motor 0 crated Valve

MOV

JODbi 1it

7 t

Ins ection Sco

e

71707

The inspector

observed surveillance test 2-SI-4.5.F.l.c,

Reactor

Core

Isolation Cooling (RCIC) System Motor Operated

Valve

(MOV) Operability.

Observations

and Findin s

The inspector

observed

the performance of'he

RCIC system

MOV

operability surveillance test

on January

7,

1998.

The purpose of this

test was to determine the operability of the

RCIC system

and to ensure

conformance with Technical Specification (TS) 4.5.F. l.c and 1.0.MM.

TS

. 1.0.MH implements the requirements

for Inservice Testing of the American

Society of Mechanical

Engineers

Code Class 1.2,

and 3 components.

The inspector verified that the procedure

used for the test

was approved

and met the requirements

of the TS.

The inspector

observed that the

prerequisites

for conducting the test were met and the appropriate

TS

Limiting Condition for Operations

were entered.

The inspector verified

that the timing values

recorded

and. the process of obtaining the values

were correct

and within acceptable limits per the procedure.

The measured

stroke time of one valve was less than the maximum

allowable,

but more than the normal range.

The inspector

observed that

the operator

misread the procedure

and thus did not recognize that the

valve needed to be restroked

and timed.

The operator timed valve 2-FCV-

71-6A,

RCIC Steam Line Drain Inboard Isolation valve,

as 2.9 seconds

in

the open direction.

This value was outside the normal

range of 0.8- 2.6

seconds,

but within the maximum allowable value of 3.4 seconds.

The

procedure indicated that the valve should

be stroked again.

The next

three steps in the procedure

described the restroke timing sequence to

be performed

when the conditions were met necessitating

that the valve

be restroked.

The operator misread the guidance

and determined these

steps to be nonapplicable.

The

NRC inspector discussed

the procedure

guidance with the operator.

The operator, after additional

review of

the procedure.

performed the restroke timing and recorded the data

according to the procedure.

The inspector noted that the licensee's

procedures

require

a detailed

review of the surveillance

packages

following testing to identify errors

such

as the one described

above.

01.3

The inspector

observed the completion of the surveillance

and the review

of the surveillance

package

by the Unit Supervisor.

.The inspector

found

no further discrepancies.

Conclusions

Overall conduct of the surveillance test

was adequate.

Poor

attention'o

detail during

a portion. of the test

was identified by the inspector.

The operator did not closely read

a procedure

step

and consequently

misunderstood

the actions necessary

after

a valve stroke time was

determined to be outside the normal

range.

Observation of Reactor

Core Isolation Coolin

Rated

Flow Test

Ins ection Sco

e

71707

The inspector

ob'served the performance of 2-SI-4.5.F.l.d,

RCIC System

Rated Flow at Normal Operating

Pressure

surveillance test.

Observations

and Findin s

.On January

7,

1998. the inspector

observed the performance of

surveillance test 2-SI-4.5.F.1.d,

RCIC System

Rated

Flow at Normal

Operating Pressure.

The purpose of this surveillance test

was to

.determine the operability of the

RCIC system in conformance with the

requirements

in TS 4.5.F. l.d and 4.5.H.3.

This test is also performed

to provide data

used to evaluate the

RCIC pump performance for ASHE

Section

XI requirements,

specified in TS 1.0.HH.

The inspector verified that the procedure

used during the performance of

the test

was

an approved

procedure

and met the TS requirements.

The

inspector

observed that the required

TS Limiting Conditions for

Operation were entered while conducting this surveillance.

The inspector attended the pre-evolution briefing and noted that the

personnel

requi red by the procedure

were present.

The brief was

conducted in the Unit 2 Control

Room.

The briefing discussed

the

precautions

and limitations. radiological controls.

and reminders of

good operating techniques.

The inspector

observed that the briefing did

not address

an overview of the test or each individual's specific

involvement in the test.

The impact of not addressing

these specifics

during the briefing subsequently

became evident.

Personnel

located in

the

RCIC turbine room did not fully understand

the scope of testing

being performed

and consequently

a delay in testing occurred.

The

inspector

noted that the Unit Operator

did not use

a briefing checklist,

such

as the list in Site Standard

Procedures

12.1,

Conduct of

Operations,

section 3.6, entitled Evolution Briefings.

After the

RCIC turbine was started

and the specified

pump discharge

pressure

and flowrate were established,

the inspector

observed that the

indicated

RCIC pump discharge

pressure

was cycling periodically above

and below the specified value.

The procedure stated that the flowrate

02

02.1

be established

at or above the specified value.

The inspector

questioned

the Unit Supervisor whether, the indicated flowrate was

acceptable for the test.

The Unit Supervisor

observed the flowrate and

decided to have the operator establish

a slightly higher flowrate.

These observations

were discussed

with the Operations

Manager

.

Subsequently,

a Problem Event Report

(PER)

was initiated addressing

the

issues

described

above.

Management

indicated that plant policies

and'ractices

regar ding reading these type of indications would be reviewed..

The inspector verified that all acceptance criteria data

was

satisfactory, all equipment

used to perform the test was within the

calibration periodicity, and that the ultrasonic flow detector

was

correctly installed, with the proper test parameters

loaded into the

computer.

The inspector

observed

personnel

in the RCIC turbine

room and

noted that

some copies of the test being used to perform steps in the

procedure

were marked

as information only, while others

were not.

The

master

copy, which was located in the Unit 2 Control

Room,

was not

marked

as

a master

copy.

Conclusions

The surveillance test

was completed satisfactorily.

The briefing before

the test

was not thorough in that it did not include an overview of the

test

and did not address

specific actions of personnel

involved in the

test.

The operator initially established

a pump flowrate

and due to

.indicated fluctuations, it was not clear to the inspector that the

specified

minimum value was met.,

This was later corrected.

Operational

Status of Facilities and Equipment

Hi h Pressure

Coolant In'ection

S s

em Walkdown

Ins ection Sco

e

71707

The inspector

performed

a detailed

system walkdown of the Unit 3 High

Pressure

Coolant Injection (HPCI) system in accordance

with Inspection

Procedure

71707.

Portions of the Unit 2 HPCI system were also reviewed.

Observations

and Findin s

Checks of all accessible

valves

showed

an overall

good material

condition.

System valves

and breakers

were positioned

as required by

system procedures.

No excessive oil leakage

was noted from system

components.

Inspection of the interior of the

HPCI relay cabinets for

Units 2 and 3 showed that no jumpers were present.

Conditions of the

interior of the cabinets

was good.

A piping support for a vent line for the Suppression

Pool Outboard

Suction

(3-FCV-073-27) valve was not properly installed and hanging from

piping.

This deficiency was previously identified by the licensee

and

a

work request to correct the deficiency had been written.

The inspector

questioned

whether the deficient piping support

posed

an operability

concern.

The system engineer

found that

PER 970918 was written to

investigate the. pipe hanger discrepancy.

The

PER determined that the

discrepancy

did not affect oper ability and that the hanger

had not been

reinstall'ed following valve maintenance

on an adjacent

check valve.

The

work to correct the discrepancy is scheduled

for the next planned

system

outage in February

1998.

While reviewing Unit 2 HPCI system,

the inspector

noted that the Gland

Seal

Exhauster suction coupling was different than the one used

on

Unit 3.

Although it was apparent that Unit 3 couplings were flexible as

discussed

in the

FSAR, it was not clear to the inspector that the Unit 2

coupling was flexible.

The system engineer

was notified of these

differences

and subsequently verified that the coupling was in fact

flexible and was part of the original design.

The coupling used

on

Unit 3 HPCI system

was of a newer design.

A steam packing leak from the turbine inlet steam trap inlet isolation

valve (3-SHV-73-'592) was observed to be blowing steam near

an electrical

junction box for the HPCI system

(3-JBOX-073-3134).

The box appeared

sealed

and contains

a drain hole as required.

The leaking valve had an

open work request.

Discussions with the system engineer indicated that

he was knowledgeable

about the packing leak and was monitoring the

status periodically.

The licensee

subsequently

installed

a temporary

herculite barrier to protect the junction box.

c.

Conclusion

The portions of the Unit 3 HPCI system reviewed were in conformance with

plant instructions.

Overall material condition was good.

The licensee

was adequately identifying and pursuing corrective actions for system

material condition deficiencies

such

as minor leaks.

02.2

Control

Room Deficiencies

Ins ection Sco

e

71707

The resident inspectors

reviewed the licensee's

process

and

implementation of identifying and tracking control

room equipment

deficiencies.

The inspector also performed

a walkdown of control

room

instrumentation

and indications to verify that deficiencies

were

accurately

being tracked.

The inspector

also performed

a walkdown of

the Backup Control Panels.

Observations

and Findin s

The licensee

has not established

a formalized procedure to identify and

track control

room equipment deficiencies.

Discussions with plant

, operators

indicated that previously there

was

a standing

order which

contained

guidance.

The guidance is currently still used

even though

the standing order is no longer in use.

The licensee defines

a control

room deficiency as

a problem with a control or indication in the control

room or remote equipment which fails to operate

from the control

room

7

point of control.

Control

room deficiencies

which have

a work request

(WR) submitted are broken into the following three work categories:

~

Control

room WR's which can be worked at steady state

100K power

~

Control

room WR's which require

a load reduction to work

~

Control

room WR's which require

an outage to work

The control

room

MR list is audited weekly in accordance

with the

guidance

and the operations

department activities schedule.

The

inspector

reviewed the list as contained in the licensee's

work planning

and control data

base.

The inspector

performed

a walkdown of the Unit 2

control panels to compare the list to the actual control

room

conditions.

No additional discrepancies

were noted by the inspector.

Discussions with plant operators

indicated that there were different

interpretations for categorizing

a control

room deficiency.

The

licensee

previou'sly identified this and presently requi res the shift

manager

to approve all control

room deficiencies.

This has

reduced the

number of errors in categorizing control

room deficiencies

and improved

consistency.

Control

room deficiencies

are monitored on

a weekly basis in the plan of

the day meeting.

The plan of the day document includes

a list of WRs

that can be worked at rated power.

Trend reports of control

room

deficiencies

are also included.

The licensee

informed the inspector

that this is performed in order to increase

management's

awareness

of

control

room deficiencies

and to heighten their priority in work

planning.

The inspector

found no recent adverse'rend

in the number of

non outage or power reduction control

room deficiencies

(16 for Unit 2

and

12 for Unit 3 when reviewed by the inspector).

During attendance

at

a maintenance

department. performance indicator meeting, the inspectors

observed that control

room deficiencies

were addressed

and that

aggressive

goals

have been set.

The maintenance

department

goal is 5

deficiencies

per operating unit control

room.

The inspectors

have also

noted

an emphasis

on resolution of CR deficiencies

during refueling

outages.

The inspector noted that the Backup Control

Panel for Unit 2 had three

items that had work requests.

Two of the deficiencies

were identified

in January

1997

and the other

was identified in June

1997.

These

items

were not tracked

as control

room deficiencies

although the importance of

the Backup Control

Panel

may warrant increased priority over other plant

work requests.

Conclusion

The licensee effectively tracks

and trends control

room deficiencies.

Aggressive goals

have been set to reduce the number of control

room

deficiencies.

The inspector noted that Backup Control

Panel

deficiencies

are not included in the control

room deficiency list

although their importance

may warrant increased

awareness.

0;

08

08.1

Miscellaneous

Operations

Issues

(92901)

0 en

Ins ection Followu

Item 260 296/97-11-01,

Status

Control Issues.

On October 21,

1997, the

icensee identified that all inputs from the

control rod drive

(CRD) temperature

recorders to the

CRD Unit High

Temperature

annunciators

in the Unit 2 control

room were disabled.

The

licensee's

investigation determined that the alarms for each point would

be turned off if a change, of the range data

was performed for that data

.

point on the recorder.

If an individual was viewing (not making program

changes,

only viewing) the range settings for any or all channels

on the

HR2500E Yokogawa recorder,

and exited the setup

menu by pressing the

"enter" and "end" softkeys rather than "aborting," then the recorder

would still view this action as

a channel

setup

change.

Although the

current range data information would be retained,

the alarm setup would

default to the "off" or disabled

mode.

The licensee indicated that an

individual performing

a scan of the range data could have inadvertently

disabled the points.

The licensee attributed the event to the lack of

clarity in the vendor technical

manual for the recorder

.

The inspectors

reviewed the licensee's

planned corrective actions

associated

with the disabled

CRD alarms.

Corrective actions

included

re-enabling the

CRD high temperature

alarm functions, briefing the

Instrument Maintenance

and Operations

personnel

to heighten the

awareness

associated

with recorder

program response to viewing program

data,

revising Yokogawa controlled vendor manual to clarify the setup

mode operation of HR 2500E

Yokogawa recorders,

evaluating training

course

ICT 103.010L

(Yokogawa Recorder

Programming

Lab Guide)

and

addressing

deficiencies,

and evaluating the availability / use of tamper

indicating devices

on Yokogawa keylock switches.

The Final Safety Analysis Report specifically addresses

that the control

rod drive temperature light is provided in the control

room to allow the

operator to know the condition of the Control

Rod Drive Hydraulic

System.

The

FSAR also specifically addresses

these

recorders

(2-TR-85-7A and 2-TR-85-7B) and the trip settings.

The inspectors

noted

that the Integrated

Computer System provides indications of elevated

CRD

temperatures

in the

CR independent of these

recorders.

Temperatures

above the alarm setpoint are printed out on an alarm typer in the

CR.

The inadequate

procedural

guidance for work on this quality related

recorder

caused

the alarms for each point to be turned off.

This is

a

violation of 10 CFR 50 Appendix B, Criterion

VS Instructions,

Procedures,

and Drawings.

This licensee-identified

and corrected

violation is being treated

as

a Non-Cited Violation, consistent with

Section VII.B.1 of the

NRC Enforcement Policy (Non-Cited Violation

260/97-12-01,

Inadequate

Procedural

Controls

on

CRD Temperature Alarms).

The IFI will remain open for additional

review of status control issues.

Conduct of Maintenance

II. Maintenance

Ml.1

Loo

A Residual

Heat

Removal

RHR

Dischar

e Pressure

Switch

Calibration.

Ins ection Sco

e

71707

The inspector observed the performance of 3-SI-4.2.B-54,

Core

Standby'ooling

System Residual

Heat

Removal

(RHR) Loop A Calibration

surveillance.

Observations

and Findin s

On January

8,

1998, the inspector observed 3-SI-4.2.B-54.

RHR Loop A

Discharge

Pressure

Calibration surveillance.

This procedure is intended

to satisfy the calibration requi rements specified in TS tables 3.3.B and

4.2.B.

The inspector verified that the procedure

was approved

and that

equipment

used

was within the calibration period.

The inspector

observed that the surveillance

was conducted satisfactorily.

The

workers used

good work practices

employing

a reader-performer

method to

perform each step of the surveillance,

and good communications

were

noted throughout the evolution.

The inspector observed that the workers demonstrated

good ownership by

submitting recommendations f'r procedure

improvements after the

surveillance

was complete.

The workers noted that the sequence

of

steps.

during thk restoration part of the procedure.

should

be changed

to improve the procedure.

The inspector

observed.

during review of the

data

recorded in the procedure,

that no order of magnitude

was provided

for an acceptance criteria value.

The acceptance criteria specified

millivolts but this was not recorded

on the data table.

The worker

appropriately

added this information and submitted

a procedure

change.

During the acquisition of the test equipment.

the inspector

observed

that the equipment did not have foreign material exclusion

(FME)

protective coverings installed.

This condition was also noted

on

equipment located

on storage

racks

and calibrated high accuracy pressure

gages.

The licensee

subsequently

placed

FME covers

on the equipment.

The licensee

discussed

with the inspector that additional evaluation

would be performed regarding implementation of FME protection

on test

equipment.

c.

Conclusions

The

RHR Loop A Discharge

Pressure

Calibration was performed

satisfactorily and good worker practices

were used during the

surveillance.

Some test equipment

was observed to not have foreign

material exclusion protection.

10

Emer enc

Diesel Generator

12-Year Maintenance

Outa

e

Sco

e

62707

The resident inspectors

observed training activities,

maintenance

activities,

and the control of contractors

during the 12-Year

maintenance

outage

on the

3C Emergency Diesel Generator

(EDG).

Observations

and Findin s

Good preparation

and detailed planning for the scheduled

outage

activities was evident.

The licensee

planned

and implemented

a post-

work lessons

learned.

The inspector

noted good maintenance

practices

were implemented

such

as cutting old 0-rings to prevent inadvertent

reuse.

The inspector

observed that foreign material exclusion covers

were used

when appropriate.

Minor issues

were identified with the

control of contractors

from a security aspect.

The training of contract

workers using

a surplus diesel

generator

in the

training center

was

a good initiative.

The inspectors

also noted that

effective use of mockup training was evident during implementation of

the power range neutron monitoring modification which was installed in

Unit 2 during the Fall

1997 outage.

.On January

13,

1998. while observing the implementation of the Fuel

Transfer Strainer Inspection which 'is proceduralized

by Mechanical

Preventive Instruction,

MPI-0-082-INS005,

Standby Diesel

Engine Twelve

Year Inspection,

the inspector

noted that the inspection

was performed

differently on the two strainers.

It appeared to the inspectors that

the procedural

requirements

were not being met.

The inspector discussed

the observation with the contractor

and brought the issue to the

attention of the TVA mechanical

maintenance

supervisor present at the

diesel.

The following day, the senior resident inspector discussed

the

observation with the Maintenance Superintendent

who had not been

made

aware of the issue.

Subsequently,

the inspector

discussed

the issue

with the Lead Mechanical

Maintenance representative

for. the diesel

outage

who indicated that the implementation of the fuel transfer

strainer

inspection did not meet the licensee's

expectations

and that

the inspection of one of the strainers

had been reperformed.

Technical

concerns with the adequacy of the

3C strainer inspections

were later

resolved through discussions

with the Mechanical

Maintenance staff.

On January

22,

1998, the inspector questioned

the initiation of a

problem evaluation report

(PER)

on this issue.

The licensee

recognized

that

a

PER had not been written and immediately initiated BFPER980095.

The licensee indicated that they believed that an oversight

had occurred

since the diesel

outage maintenance

logbook had indicated their

intention to write a

PER.

The inspectors

were also concerned that the

maintenance

personnel

did not raise the issue to the appropriate levels

of management

prior to

NRC discussion with the Maintenance

Superintendent.

Since

a

PER was not initiated, the Management

Review

Committee did not review the incident prior to the

EDG being returned to

11

service.

The inspectors

have documented

examples

where

PERs

have

requi red prompting in the past

(see

IR 259,260,296/97-11

and

IR

259,260,296/97-07

).

The failure to promptly document the

NRC

identified condition using the licensee's

Corrective Action Program

and

report it to appropriate levels of management

is

a violation of

SSP-3.4,

Corrective Action Program.

(Violation 296/97-12-02.

Failure to

Document Condition Adverse to Quality)

Conclusions

Good preparation

and detailed planning for the scheduled

outage

activities was evident.

The training of contractors

using

a surplus

diesel generator in the training center

was

a good initiative.

Minor

issues

were identified with the control of contractors

from a security

aspect.

A violation of regulatory requirements

was identified regarding fai lure

to document

a condition adverse to quality identified by the

NRC.

Surveillance Testin

Ins ection Sco

e

61726

The inspectors

reviewed completed surveillance instructions for selected

.instruments to verify that the surveillance instructions satisfied the

Technical Specification calibration and functional testing requirements.

Observations

and Findin s

The inspectors

reviewed completed surveillance instructions for the most

recent performance of instrument calibration

and functional testing for

the Unit 2 Drywell "A" Channel

High Pressure

Scram

and Unit 2 "A"

Channel

Scram Discharge

Tank High Water Level. Scram.

The inspectors

also reviewed documentation

associated

with those

sur vei llances

performed prior to the Unit 2 restart in 1991.

Completed licensee

surveillance instructions

reviewed included the following:

2-SI-4.1.B-5(A)

Reactor Protection

and Primary Containment

Isolation System High Drywell Pressure

Instrument

Channel Al Calibration.

2-SI-4. 1.A-ATU(A) Reactor

Protection

and Primary Containment

Isolation System Analog Trip Unit Channel Al

Functional Test.

2-SI-4.1.B-8(A)

RPS High Water Level in Scram Discharge

Tank

Calibration.

2-SI-4.1.A-8(A)

RPS High Water Level in Scram Discharge

Tank

Functional Test.

C.

H3

H3.1

12

Instrumentation calibrations were required

by TS to be performed every

18 months while channel

functional tests

were required monthly.

The

inspectors

also reviewed

TVA Engineering Calculations,

NESSD 2L-085-

0045A, Setpoint

and Scaling

Document,

2-LE-85-45A and 2-LS-85-45A,

Scram

Discharge

Tank High Water

Level Scram,

and

NEESD 2P-064-0056A-00-01,

Setpoint

and Scaling

Document,

2-PT-64-56A and 2-PIS-64-56A.

High

Drywell Pressure

Scram,

which provided the engineering

basis for the

licensee's. setpoint scaling methodology.

Additionally. the inspectors

reviewed the applicable instrument calibration data sheets

from

Instrument Maintenance

Procedures.

2-SIMI-85A, Scram Discharge

Tank

Setpoint

and Scaling

Document,

and 2-SIMI-64A, Primary Containment

Setpoint

and Scaling

Document.

These instrument calibration data sheets

were used

by the licensee's

maintenance

organization to provide the

instrumentation technicians with reference

data for use during

instrument calibrations.

No deficiencies

were identified during this

review.

The inspectors

noted that setpoint values

used in the

instrument calibration and functional tests

were consistent with the

allowable values

from the licensee's

setpoint

and scaling

documents

and

the Technical Specifications.

Conclusions

No deficiencies

were identified during the review of selected

completed

instrument calibration and functional testing documentation.

The

.inspectors

concluded that setpoint values

used in the licensee's

instrument calibration and functional tests

were consistent with the

. allowable values

from the licensee's

setpoint

and scaling

documents

and

the Technical Specifications.

Maintenance

Procedures

and Documentation

Review of Work Order Packa

es

Ins ection Sco

e

62700

The inspectors

reviewed Work Order

(WO) packages to determine the

adequacy of the licensee's

process for planning,

accomplishing. testing,

and -documenting the work activities

and to verify that the documentation

satisfied the requi rements

from Licensee

Procedures

SSP-6.2,

Maintenance

Management

System,

and SSP-7.1,

Work Control.

Observations

and Findin s

The inspectors

reviewed various

WOs, completed

and closed during 1991,

1993,

and during the period of July

1 - December

31,

1997, for WO

adequacy

and implementation.

The inspectors

reviewed documentation

for

the following completed maintenance activities:

WO 90-00071-00,

Replace 'diaphragm in CRD Scram Inlet Valve, 2-FCV-

085-39A/1035

WO 90-00055-00,

Replace

diaphragm in CRD Scram Inlet Valve, 2-FCV-

085-39A/0235

P2.2

26

The inspector

used

EPIP 17.

Emergency

Equipment

and Supplies.

Revision 21, to evaluate the inventories of emergency cabinets

and

lockers in the

TSC and

OSC.

The equipment tested

by the inspectors

operated satisfactorily

and the emergency

lockers inventories

were

complete.

The inspector

reviewed documentation of completed inventories

from

December

1996 through

December

1997.

The inspectors

found the

documentation

complete.

In the event of a complete loss of communications to the site, the

licensee

had added

a satellite phone in the TSC.

The equipment

supporting the satellite

phone was placed in an independent,

secure

cabinet

and provided an independent

power supply.

Conclusion

The inspector

concluded that the licensee satisfactorily maintained the

Emergency

Response Facilities and equipment.

Equipment tested

by the

inspector

performed satisfactorily. Audits of equipment

and supplies

were completed at the required frequencies.

Communication capabilities

were enhanced

by the addition of a satellite

phone.

Public Alertin

S stem

a.

Ins ection Sco

e

82701

This area

was inspected to review the licensee's

method of notifying the

public in the event of an emergency.

and the Public Alerting System test

frequency

and test data.

Requirements

applicable to this area

are found

in 10 CFR 50.47(b)(5),

Sections

IV.D of Appendix

E to 10 CFR Part 50,

and the licensee's

Emergency

Plan.

Observations

and Findin s

The licensee

maintained

100 sirens within the Emergency

Preparedness

Zone for their public alert and notification system.

The inspectors

reviewed documentation

from December

1996, through

December

1997, for

the bi-weekly si lent tests,

monthly sounding

and an annual

sounding of

the sirens.

The inspectors

determined that the sirens

had been tested

at the requi red frequencies.

The 1996 Browns Ferry Nuclear Plant siren

availability report summary indicated

a siren availability of 98.9

percent

compared to the Federal

Emergency

Hanagement

Agency's acceptance

criterion of 90 percent.

The inspector

met with the individual responsible

for maintaining Browns

Ferry sirens.

The inspector

reviewed documentation

and discussed

the

quarterly and annual

maintenance of the sirens.

The documentation

indicated that as

a system,

the sirens

needed

minimal repairs.

The

licensee

maintained

a matrix which gave

a quick, visual indication of

individual si ren performance for trending purposes.

The matrix was

a

positive TVA initiative.

27

In addition to the sirens,. the licensee maintained tone alert

radios for area

schools

and day care centers.

Documentation

reviewed by the inspectors

indicated that the licensee

satisfactorily distributed

and maintained the tone alert radios.

Conclusion

The inspector

concluded that the siren system

and tone alert radios were

being satisfactorily tested

and maintained.

The licensee

was

effectively trending siren operability.

EP Procedures

and Documentation

Emer enc

Plan

Im lementin

Procedures

Ins ection Sco

e

82701

The inspector

reviewed the changes to the Emergency Plan.

selected

EPIPs,

and evaluated

whether changes to the EPIPs were in agreement with

and implemented the Emergency

Plan.

Requirements

applicable to this area

are found in 10 CFR 50.47(b)(16).

10 CFR 50.54(q),

Appendix

E to 10 CFR Part 50,

and the licensee's

Emergency

Plan.

Observations

and Findin s

The inspector

reviewed

EPIP 14, Radiological Control Procedures,

Revision 13, effective date of November 17,

1997.

The procedure

was used

by on shift personnel

to perform a manual offsite dose

assessment

in the

event of a radiological

emergency.

The inspectors specifically focused

on EPIP 14. Attachment

E.

"Manual Methodology For Projecting Total

Effective Dose Equivalent

(TEDE)" a computer

method

and

a manual

method.

If the computer

was not available,

then the manual

method

was to be

used.

It was the licensee's

expectation that both methods

should give

the user the same result.

The inspector

requested

and observed the

licensee

use the same input data

and perform an offsite dose calculation

using both the manual

and computer

methods.

The inspector 's review of

the calculations

noted that results

compared favorably.

The inspector

reviewed Revisions

32, 33, 34, 35,

and 36 to the

licensee's

Emergency

Plan.

The inspectors

noted that the changes

were mainly clerical or organizational

changes

which did not

decrease

the effectiveness

of the Emergency

Plan.

The inspector verified that all letters of agreement identified in

the Emergency

Plan were current.

The inspector verified by reviewing

a letter dated July 11,

1997,

that the State

had performed thei r required

annual

review of the

Emergency Action Levels.

The inspector

reviewed the licensee's

March 5,

1997, Notification Of

Unusual

Event

(NOUE) emergency declaration

based

on Unit 3 loss of

28

station

power during

a refueling outage.

In evaluating the licensee's

response

to the event, the inspectors

reviewed the licensee's:

EPIP-1,

Emergency

Plan Classification Matrix.

EPPOS 2, Timeliness of Classification of Emergency

Conditions

Post

Event Review,

Problem Evaluation Report:

BFPER970486

Unit Status

(Refueling)

normal

"day shift" Control

Room staffing and

Operations

Department

document,

"Conduct Of

Operations" which included duties

and responsibilities

of key personnel

during abnormal

and emergency

conditions.

The loss of power occurred at 10:40 a.m.

The notification of

Unusual

Event

(NOUE) was based

on the Emergency Action Level

(EAL)

5.1-U: "loss of off-site power for greater than

15 minutes".

Therefore, station power was lost for 15 minutes before the

conditions for the

EAL were met.

The event was declared at ll:22

a.m.,

27 minutes after meeting the conditions for the

EAL or 42

minutes after loosing station power.

NRC guidance provided to the

industry in EPPOS-2,

"Timeliness of Classification of Emergency

Conditions" indicates

15 minutes

as reasonable

period of time for

.assessing

and classifying

an emergency

once indications are

available to control

room operators that an

EAL has

been

exceeded

and the licensee's

Emergency

Plan Implementing Procedure

(EPIP)-l,

Emergency

Plan Classification Matrix, states that

a declaration

needs to be made within 15 minutes of'vailable indication (10:40

event/10:55

EAL was met).

The inspectors'eview

of the documents

listed above determined that:

Unit 3 was. shut

down (refueling).

Sufficient operations

personnel

were available to

effectively respond to the event

and implement the

actions of the licensee's

Emergency

Plan.

The licensee's

"Conduct of Operations"

document

clearly delineates

control

room staff action and

responsibilities

during abnormal

and emergency

conditions.

The licensee

concluded that the event declaration

was timely,

although it exceeded

the guidance in EPPOS-2

and EPIP-1.

The

licensee's

basis f'r not meeting the 15 minute guidance

included

the need to: notify key management:

dispatch

personnel

considerable

distances to the cooling tower switchgear

and

161

KV

switchyard; wait for feed back from dispatched

personnel:

and

respond to the notification of a tornado watch.

The licensee's

review did not address

why the condition could not be adequately

identified from the control

room instrumentation,

without the need

for feedback

from the switchyards.

The

EAI

was objective and

unambiguously written, and established

the criteria for

p5

P5. 1

29

classification.

The licensee's

review did not evaluate the

relative priority of'ey management notification to the inherent

need to rapidly communicate

emergency conditions.

and whether the

shift staffing was most efficiently utilized.

The licensee

did

not identity any lessons

learned

on timeliness.

It was not clear

to the inspector

that the licensee's

evaluation

was self-critical

and that

a

sufficient explanation for the delay was provided.

Conclusion

Dose assessment

results

from the manual

procedure

used

by on shift

personnel

compared favorably to the computer

method for dose

assessment.

Revisions

32.

33. 34, 35.

and 36 of the Emergency

Plan were made

in accordance

with requirements.

The

NRC and licensee

goal for declaration of an emergency classification

within 15 minutes of event recognition was exceeded

by 12 minutes during

the loss of station

power event

on Narch 5,

1997.

It was not clear to

the inspector that the licensee's

evaluation

was self-critical and that

a sufficient explanation for the delay was provided.

Staff Training and Qualification in EP

Trainin

of Emer enc

Res

onse Personnel

Ins ection Sco

e

82701

The inspector

reviewed the Emergency

Response

Training Program to

evaluate the current qualification of the emergency

response

personnel

and their training.

Requirements

applicable to this area

are contained

in 10 CFR 50.47(b)(2)

and (15), Section

IV.F of Appendix

E to 10 CFR Part 50.

and the licensee's

Emergency

Plan.

b.

Observations

and Findin s

The licensee

continued to maintain classroom training of the Emergency

Response

Organization

(ERO) in accordance

with Section

15 of the

Emergency

Plan and

EPIP 19, "Radiological

Emergency

Preparedness

Training and Drills."

The inspector

reviewed three lesson

plans

and their associated

exams

identified in the matrix.

The inspectors

determined that the lesson

plans were well organized

and the subject matter'ontent

was

commensurate

with the position being taught.

The exams were generally

well written and adequately

challenging for the position.

The status of ERO training was reviewed by selecting approximately

twenty individuals from the

ERO roster

and verifying their

training was current based

on the licensee's

computer system.

The

inspectors

compared the training dates

indicated

on the computer

against the class

attendance

roster

.

No discrepancies

were found.

Conclusion

30

P5.2

P7

P7.1

The

ERO training program was satisfactory.

ERO lesson

plans were good,

and exams were adequately challenging.

Emer enc

Plannin

Drills

Ins ection Sco

e 82701

The inspector

reviewed the licensee's drill documentation to

evaluate'hether

they were conducting the types

and number of drills identified

in Section

14, "Drills and Exercises," of the licensee's

Emergency Plan.

Requirements

applicable to this area

are contained in 10 CFR 50.47(b)(14),

Section IV.F(1) of Appendix

E to 10 CFR Part 50.

Observations

and Findin s

The inspector

reviewed

1996 and

1997 documentation of Browns Ferry

quarterly TSC/OSC staffing drill with each of the three teams;

PASS

Drills; and Medical Drills with Huntsville Hospital

and Athens-Limestone

Hospital.

Each of the three teams;

Red.

Blue.

and Green, participated

in an equal

number of drills.

The 'inspector verified that in 1996 and

1997 the licensee

had conducted

~ the required drills in accordance

with Section

14, "Drills and

Exercises," of their Plan.

The licensee

used the training simulator to conduct

ERO drills.

Since

the last inspection,

the licensee started

conducting

"Post Drill

Critique Table Top" drills with the. team that had just participated in

the simulator controlled drill.

The licensee training philosophy was

that, if the team were briefed on the critique findings and the same

teams

re-,enacted

the scenario in a table top walkthrough, the ensuing

dialog within the team. of actual

response

and expected

response,

could

enhance their performance.

The inspectors

considered

the table top

drills a program strength.

The inspectors

noted that "Post Drill

Critique Table Top" drills were not

a requirement in the Emergency

Plan

or EPIPs.

Conclusion

The licensee satisfied the drill commitments in their Emergency

Plan.

Post simulator drill table top scenario walkthroughs were

a program

strength.

equality Assurance in EP Activities

Re uired

10 CFR 50.54 t

Audit of Emer enc

Pre aredness

Pro

ram

The inspector

reviewed this area to assess

the quality of the required

audit and evaluate

whether

the audit met the requirements of

10 CFR 50.54(t)

and the licensee's

Emergency

Plan.

Observations

and Findin s

31

P7.2

Audit SSA9703

was

a combined audit for Browns Ferry.

Sequoyah,

Watts Bar

Nuclear Plants,

and Corporate Offices in Chattanooga

and Knoxville,

conducted

between

June

16 and August 1,

1997.

The audit team consisted

of a Lead Auditor and eleven

team members

from the TVA nuclear, sites,

TVA corporate,

and

a member from another utility.

The audit did not

identify any weaknesses

or

PERs in the Emergency

Preparedness

Program at

Browns Ferry.

One weakness

was identified for Browns Ferry in the area of

Meteorological

Programs

regarding the calibration acceptance

criterion for the meteorological

wind speed

sensors.

Conclusion

The inspector's

review concluded that the Emergency

Preparedness

audit

was organized

and objective and satisfied the requirements

in

10 CFR 50.54(t).

Licensee's

Corrective Action Pro ram For Drill Comments

and Issues

Ins ection Sco

e

82701

This area

was reviewed to evaluate the licensee's

corrective actions to

comments

and issues identified in their drills. Requirements

applicable

to this area

are contained in 10 CFR 50.47(b)(14).

b. Observations

and Findin s

The inspector

reviewed findings from the licensee's drill critiques

and

verified that drill comments

were being tracked

on Problem Evaluation

Reports

(PERs), the plant wide tracking system,

and Activities

Management

Oversight System

(AMOS),

a local

PC based tracking system

used

by the Emergency

Preparedness

groups.

From the tracking lists, the

inspector selected

four items that had been closed.

and reviewed the

documentation to evaluate the licensee's

timeliness of closure

and

quality of thei r resolution.

The closed

items reviewed by the inspector

were satisfactorily resolved

and closed in a timely manner.

Conclusion

The inspector concluded that the licensee

was satisfactorily

tracking and resolving drill comments.

32

'adiological

Protection

and Chemistry Controls

Tr ans ortation of Radioactive

Hater ials

Ins ection Sco

e

86750

and TI2515/133

The inspectors

evaluated

the licensee's

transportation of

radioactive'aterials

program for implementing the revised Department of

Transportation

(DOT) and Nuclear Regulatory Commission

(NRC)

transportation

regulations for shipment of radioactive materials.

The

regulations

are published in 10 Code of Federal

Regulations

(CFR) 71.5

and 49 CFR Parts

100 through 177.

Observations

and Findin s

The inspectors

reviewed procedures

and determined that they adequately

addressed

the following: assuring that the receiver

has

a license to

receive the material

being shipped;

assigning the form, quantity type,

and proper shipping

name of the material to be shipped; classifying

waste destined for burial; selecting the type of package

required;

assuring that the radiation

and contamination limits are met:

and

preparing shipping papers.

The inspectors

reviewed the Certificate of Compliance

(CoC) No.5805 for

~the Model

No.

CNS 3-55 package

and

CoC No.

9168 for the Model

No.

CNS

8-120B package

and found that the licensee

was

an authorized

user.

The

inspector

reviewed the receipt surveys for the incoming package

and

found that they followed their procedural

requirements.

The inspectors

verified that prior to the shipment

made

on December

10.

1997, the

silicone 0-ring seals

were inspected,

by the licensee,

for defects

(there were none),

and the 0-rings had been replaced within six months

as required

by the

CoC No. 5805.

The inspectors

observed the cask decon

and witnessed the final surveys for this package

and the shipping papers

that were presented to the shipper

(TRI-STATE MOTOR TRANSIT) and found

no items of non-compliance.

Shipment

number

1297-7852

contained

approximately

13,000

Ci of irradiated

hardware.

The inspectors

also

reviewed the shipping paperwork for shipment

1197-7801

made

on

November 25,

1997 that consisted of approximately 10.000

Ci of

irradiated hardware

and found no items of non-compliance for either

shipment.

The inspectors

reviewed the lesson plan for the Radioactive

Waste

ackaging

and Loading Inspector Training, Revision

2 and judged them to

e adequate.

The inspectors

also reviewed the Radioactive

Waste

Packaging,

Transportation.

and Disposal training requi re by 49

CFR Part

172, Subpart

H and IE 79-19 and determined that the training met the

requirements

and there were three individuals onsite who had received

a

Certificate of Completion for the training July 8-11,

1997.

Conclusions

33

R2

R2.1

Based

on the above reviews, the inspectors

determined that the licensee

had effectively implemented

a program for shipping radioactive materials

required

by NRC and

DOT regulations.

Status of Radiation Protection

(RP) Facilities and Equipment

Occu ational Radiation

Ex osure Control

Pro ram

I

Ins ection Sco

e

83750

The inspectors

reviewed implementation of selected

elements of the

licensee's

radiation protection program.

The review included

observation of radiological protection activities including radiological

postings; verification of posted radiation dose rates

and contamination

controls within the Radiologically Controlled Area

(RCA).

The

inspectors

also reviewed selected

Problem Evaluation Reports

(BFPER).

Observations

and Findin s

The inspectors

toured the reactor building including the refueling

floor, radwaste facilities, and outside yard areas

including radioactive

material storage

areas.

At the time of the inspection,

radiological

housekeeping

was observed to be good. Radiologically controlled areas

observed

were appropriately posted

and radioactive material

observed

was

appropriately stored

and labeled.

The inspectors

independently verified

dose rates of posted

boundary

ropes

on the refueling floor and found the

dose rates

as noted

on the surveys

and as posted.

The inspectors

reviewed

BFPER971425,

dated

September

11,

1997, involving

a slightly contaminated scaffold jack found on the bottom floor of the

Intake Building.

The jack was discovered

by the licensee

during

a

routine monthly survey of the area.

As a result'of the identification

of this jack

~

an aggressive

search of the scaffolding and scaffolding

hardware located outside the plant was initiated by the licensee.

Two

other items were identified as having

a small but detectable

quantity of

contamination during this search.

The licensee

performed

a cause

analysis to determine

how the material got outside the radiological

control area

(RCA) and determined that improper removal

was the apparent

cause.

The licensee instituted

an eight step corrective action program

to prevent recurrence.

The inspectors selectively toured the site and

did not find any additional instance of similar material.

The

inspectors

observed that.

as stated in the corrective actions, scaffold

material

used

or stored outside of an

RCA was in the process of being

painted green to fulfillthe commitment

"GREEN is CLEAN".

The

inspectors

reviewed the licensee's

summary of events in the last two

years that was attached to the

PER and found two additional

PERs,

BFPER

970717

and

BFPER 971340, that addressed

particles

found inside the plant

but outside the

RCA.

The first had

a count rate so low that the

licensee

was unable to detect the particle in several

locations in the

PCN-1B.

The second particle most likely came from a worker going to a

I

decon

shower

and was not found in the backtrack survey.

The licensee

added guidance to procedure

RCI-1 on precautions for transport of

contaminated

material through clean areas.

Contamination results

from

counts of selected

swipes,

by the inspectors,

from "clean areas"

were

found acceptable.

Conclusions

Radiological conditions in radioactive waste storage

areas

were observed

to be good.

Material

was labeled appropriately

and areas

were properly

posted.

In addition,

RADCON PER(s) were aggressively

evaluated,

cause

analysis

performed

and corrective measures

to prevent recurrence

instituted.

Li uid Effluent Radiation Monitors and Li uid Waste Treatment

S stem

Ins ection Sco e'4750

The inspectors

reviewed selected

licensee

procedures

and records for the

operation of the liquid radiation effluent monitor

and the start-up

and

operation of the liquid radwaste treatment

system

(THERMEX').

Observations

and Findin s

The inspectors

toured the radwaste facility to observe the physical

layout and operation of the process

and radiation monitors in use.

The

inspectors

reviewed the effluent liquid radiation monitor operational

history and repair work orders

and observed that monitor 0-RM-130 had

recent occurrences

of spiking during plant releases.

Resolution of work

order

WO 97-007660-00

was reviewed

and the spiking was attributed to

electrical spikes.

During the inspection the licensee also discussed

that

a leaking drain valve had lowered the liquid level in the tank that

was monitored by the detector

and thus altered the background

(higher

than normal) so that when effluent liquid filled the monitored chamber

the count rate was lowered because of the higher density of the liquid

vs. the air density when the chamber

had

a reduced liquid volume.

The

drain valve was replaced to correct the altered background settings.

Additional

NRC review of this issue is documented in Inspection Report

97-11.

The licensee

made one of two total liquid releases

in November to

verify monitor operabi lity.

During the period of investigation

compensatory

measurements

as permitted

by the Offsite Dose Calculation

Manual

(ODCM) were in place to ensure that no unmonitored

releases

were

made.

The inspectors

reviewed the liquid release

data for the period

January

1997 thru December

1997 and observed that the peak

number of

releases

occurred in March (32) and the least

number of release

occurred

in November (2).

One of the November releases

was

a release to verify

the operabi lity of the liquid effluent monitor.

The Total Effective

Dose Equivalent for liquid release for the year to date

was calculated

to be approximately 0. 15 mrem or about 4.9X of the

ODCM annual limit of

3.0 mrem.

The inspectors

reviewed logsheets

564. 1.

EPA DATA LOGSHEET,

for the period June

1997 thru November

1997

and the Turbidity Work Sheet

683-1 for the same period to ensure that no liquid effluents

exceeded

35

release limits.

There were no anomalous turbidity samples

from a

radwaste liquid effluent batch release

containing particulates.

Turbidity was found to be less than the 1.0

NTU for those tanks

released.

The inspectors

reviewed the physical layout of the

THERMEX'system

and

reviewed the start-up

and operational

data for the system.

Several

improvements

had been

made, as

a result of lessons

learned during start-

up and were being tested for effectiveness.

One of the improvement

items was the use of available spent resin exchange capacity in High

.

Integrity Containers

HIC(s) to treat brine from the liquid system

and

the other was the addition of coagulant-aid

media to help improve the

phase separator

operation

and reduce resin fines carryover into the

Reverse

Osmosis

elements

(RO).

Some indication of resin fines had been

observed in the second

RO stage.

The inspectors

review of the

analytical results for the discharges

did not find any evidence of the

resin fines getting through the treatment

system for subsequent

release

into the environment.

Conclusions

Liquid effluent releases

reviewed during this inspection were found to

meet the regulatory requirements

and the compensatory

analysis permitted

by the

ODCM during the effluent radiation monitor 0-RM-130 outage were,

satisfactory.

Conduct of Security and Safeguards Activities

Access Authorization

Ins ection Sco

e

81700

To verify that the licensee

had an adequate

procedure

for review, if

requested

by an individual who is denied

access

or their access

is

suspended

or revoked'n

accordance with the Access Authorization (AA)

Program.

Observation

and Findin s

The inspectors

reviewed

AA records of selected

individuals to determine

that the licensee

had adequately

implemented the AA requirements

which

are to ensure that individuals who are granted unescorted

access

are

trustworthy, reliable and do not constitute .an unreasonable

risk to the

health

and safety of the public.

The inspectors

reviewed the licensee's

AA Procedure.

TVA Nuclear

Standard,

STD-11. 1, Providing Access

Clearance for Nuclear Plants

and

Safeguards

Information,

and determined that the procedure clearly

defined the AA regulatory requirements.

Appendix

B of STD-11.1

established

the criteria for denying,

suspending.

or revoking

a

clearance.

Appendix D, of STD-11. 1, established

the process

for appeal

and defined the requirements of the screening

review board.

\\

c.

Conclusi on

36

The inspectors

determined,

through AA procedures

and records

review,

that the licensee

had established

in thei r procedures

an appeals

process

and

an adjudication process to ensure that personnel

who were granted

unescorted

access

were trustworthy, reliable and do not constitute

an

unreasonable

risk to the health

and safety of the public.

There were 'no

violations of regulatory requirements

noted in this area.

V. Mana ement Heetin

s

X1

Exit Heeting Summary

The resident inspectors

presented

inspection findings and results to

licensee

management

on January

23,

1998.

Other meetings to discuss

report issues

were conducted during the report period including formal

meetings with plant management

on December

12,

1997,

and January

16,

1998.

The characterization

of an Emergency

Preparedness

issue described

in Section

P3. 1 was discussed

in a telephone

conversation

January

14,

1998.

The licensee

acknowledged the other findings presented.

Proprietary information is not 'included in this inspection report.

Licensee

PARTIAL LIST OF

PERSONS

CONTACTED

T. Abney. Licensing Manager

J. Brazell, Site Security Manager

R. Casey,

Manager,

Access Authorization/Fitness for Duty

R. Coleman, Acting Radiological Control

Manager

J.

Corey. Radiological Controls

and Chemistry Manager

T. Cornelius,

Emergency

Preparedness

and Planning

C. Crane, Site Vice President.

Browns Ferry

T. Feltman,

Emergency

Preparedness

R. Greenman,

Training Manager

J.

Johnson,

Site Quality Assurance

Manage

R. Jones.

Assistant Plant Manager

S.

Kane. Acting Site Licensing Supervisor

C. Kelly, Corporate Security Manager

R. Kitts, Manager,

Emergency

Preparedness,

Corporate

R. Moll. System Engineering

Manager

G. Little, Operations

Manager

B. Marks,

Emergency

Preparedness,

Corporate

D. Nye, Site Engineering

Manager

D. Olive, Acting Operations

Superintendent

J.

Shaw,

Design Engineering

Manager

K. Singer,

Plant Manager

J. Schlessel.

Maintenance

Manager

IP 37551:

IP 40500:

IP 62700:

IP 62707:

IP 62706:

IP 61726:

IP 71707:

IP 71750:

, IP 73756:

IP 81502:

IP 82701:

IP 83750:

IP 84750'P

86750:

IP 92901:

IP 92902:

IP 92903:

37

INSPECTION

PROCEDURES

USED

Onsite Engineer ing

Licensee Self-Assessments

Maintenance

Implementation

Maintenance

Observations

Maintenance

Program

Surveillance

Observations

Plant Operations

Plant Support Activities

Inservice Testing of Pumps

and Valves

Fitness

For Duty Program

Operational

Status of the Emergency

Preparedness

Program

Occupational

Radiation

Exposure

Radioactive

Waste Treatment.

and Effluent and Environmental

Monitoring

Solid Radioactive

Waste

Management

and Transportation

Of

Radioactive Materials

Followup-Plant Operations

Followup-Maintenance

Followup-Engineering

ITEMS OPENED

DISCUSSED

AND CLOSED

OPENED

~T

e

Item Number

NCV

260/97-12-01

VIO

296/97-12-02

Status

Closed

Open

Descri tion and Reference

Inadequate

Procedural

Controls

on

CRD Temperature

Alarms (Section

.08.1)

Failure to Document Condition

Adverse to Quality (Section Ml.2)

NCV

260/97-12-03

Closed

NCV

259,260,296/97-12-04

Closed

Inadequate

Procedure for PHT

(Section H8.1)

Design Basis

Not Translated

Properly

for RHRSW Pump Requirements

(Section

E8.1)

NCV

296/97-12-05

Closed

Inadequate

Post Modification Test

(Section H3.2)

DISCUSSED

~T

e

Item Number

.IFI

260,296/97-11-01

Status

Open

Descr i tion and Reference

Status

Control Issues

(Section 08.1)

CLOSED

T~e

Item Number

LER 260/97-005-00

LER

260/96-005-00

VIO

260/96-199-01013

VIO

260/96-199-02014

LER 259/97-004-00

IFI

.260,296/95-064-10

IFI

260/97-05-04

LER 260/96-007

Status

Closed

Closed

Closed

Closed

Closed

Closed

Closed

Closed

38

Descri tion and Reference

ESF Components

Were Actuated

as

a

Result of an Inadequate

Procedure

(Section H8.1)

Unit 2 Scrammed

on Low Reactor

Wat'er

Level

Due to the Digital Feedwater

System Reinitializing its Feed

Pump

Demand Output Signal to Zero and the

Subsequent

Trip of the Reactor

Core

Isolation Cooling on High Exhaust

Pressure. (Section H8.2)

RCIC Inoperability (Section H8.3)

Failure to Comply with IST

Requirements

(Section H8.4)

Residual

Heat

Removal Service Water

Pump Limiting Condition for

Operation is Non-Conservative

(Section E8.1)

Secondary

Containment Ventilation

Damper Failures

(Section

E8.2)

Spurious

HSIV Closures

on Reactor

Scram (Section E8.3)

Unit 2 Scram on Turbine Control

Valve Fast Closure

Due to Loss of

Excitation to Main Generator

(Section E8.4)

~y

13

WO 91-42376-01,

Troubleshoot Controller 2-FC-2-190 which would not

operate in automatic

WO 91-35689-01,

Repair valve 1-HCV-90-133A

WO 91-44533-01,

Troubleshoot noise located inside Motor 3-MTR-030-

0239

WO 91-41927-00,

Relug wires on

EDG Control Cabinet

WO 91-33796-00,

Open

and inspect wireways

and covers for Reactor

NOV Board 3A Panel

3A

WO 91-44048-00.

Clean

Fan 0-FAN-030-0186 due to low flow rate

WO 91-41654-01,

Remove

and inspect Valve, 0-CKV-067-539

'O

91-31161-00,

Torque

EDG starting air compressor

high pressure

gasket bolts

WO 91-24427-00,

Exercise various

EDG air start relief valves

WO 93-01197-01,

Install temporary

RPV level instrument

on refuel

floor

WO 97-02594-01,

Disconnect/Remove/Reinstall/Reconnect

B3

RHRSW

Pump Motor 0-NTR-023-0088

WO 97-04404-00.

Perform Inspection

and Maintenance

on

Operator

for Isolation Valve 2-FCV-071-0002

WO 97-04414-01,

Repair

Damaged

Motor Lead for 2-NTR-071-0003

WO 97-06387-49,

Repair Packing

Leak for Valve 2-FCV-071-0002

WO 97-07577-00,

Replace

Valve 2-LSV-071-0005

WO 97-08654-00,

Replace Relief Valve 0-RFV-002-3105

WO 97-08659-00,

Troubleshooting

Valve 0-NVOP-067-0049 for Failure

of Indication Light

WO 97-09218-00,

Perform Adjustments to 0-PMP-023-0088

Pump

Impeller to Achieve Proper Flow

WO 97-09807-00.

Replace

Valve 3-FSV-076-00948

WO 97-10735-01,

Replace Relief Valve 3-RFV-086-0552A

WO 97-10916-00,

Replace Relief Valve 3-RFV-086-0522D

WO 97-11249-01,

Troubleshoot failure of valve 3-FSV-090-0257A

position indication

All the

WOs reviewed contained workorder summaries,

pre-job references

and requirements,

work instructions.

material requisition forms,

descriptions of actual

work performed,

work closure documents,

and

attachments.

The work order summaries

included component

identification. problem and work descriptions,

and requirements for

post-maintenance

testing.

The required

procedures

for the tests

were

also listed in the work order summary.

Post-maintenance

testing is

further discussed

in Section M3.2.

The work instructions listed the

step by step

sequence

of the work to be performed,

depending

upon the

complexity of the work.

WO attachments

were used for recording data

and

in some instances

contained additional

procedures

used during the work

activity.

Based

on the review of the completed documentation,

the

inspectors

concluded that the licensee's

WO packages

were generally

adequate.

The planning

and work instructions

were thorough

and complete

and provided sufficient details for the craftworkers to implement the

work activity.

Additionally, the

WOs included documentation to show

that required

post-maintenance

tests

were performed

and that all

required

QC inspection holdpoints

had been completed.

c

0

14

During the review of completed

WOs the inspectors

concluded that current

and previous

programs for control of temporary jumpers

and lifted leads

associated

with maintenance

work activities was adequate.

During the review the inspectors identified several

WO documentation

deficiencies.

These deficiencies

included

a missing checkmark

and

missing step completion signatures

by craft personnel

and

a missing

cable inspection attachment.

The inspectors

concluded that the

deficiencies

were minor

and that the affected workorder packages

were

adequate.

The inspectors

discussed

the deficiencies with members of

'icensee

management.

The inspectors

were informed that the deficiencies

had not met licensee

management's

expectations.

Additionally. the

inspectors

noted that the licensee

issued

Problem Evaluation Reports

(PER)

BFPER 980071

and

BFPER 980076 to address

these deficiencies.

Conclusions

WO packages

reviewed by the inspectors

were generally adequate.

They

contained sufficient details,

work instructions.

and requirements

for

craftworker

implementation.

The work, tests,

and documentation

completed

met the stated

requirements.

Review of Post Maintenance Testin

Pro

ram

Ins ection Sco

e

62700

The licensee's

post-maintenance

test

(PMT) program was reviewed to

determine the adequacy of the licensee's

process for planning and

accomplishment of testing prior to return of equipment to service

and to

verify that the testing

had satisfied the requirements

from SSP-6.50,

Post-Maintenance

Testing.

Additionally, the inspectors

reviewed the

details associated

with a previous fai lure to perform adequate

post-

modification testing.

Observations

and Findin s

During a previous review of the licensee's

PMT process

documented

in

Section

M3.1 of Inspection

Report 50-259.260,296/97-10

the inspectors

identified a weakness.

This review identified that

PMT requirements

specified in WOs were not consistent with respect to the level of detail

and

some

WOs included descriptions of PMT requi rements

which lacked

detail.

In some cases.

additional interpretation

by maintenance

personnel

was required prior to performing the work activity.

During the review of recently completed

WOs documented in Section

M3. 1

the inspectors

reviewed the adequacy of post-maintenance

testing that

had been performed before equipment

was returned to service.

During

this more recent

review,

improvement in the

PMT planning process

was

noted.

PMT requirements

specified in these

WOs were more consistent

with respect to the level of detail

and no examples of required

additional interpretation

were noted during the review.

M3.3

15

During review of WO 97-11249-001.

the inspectors

determined that the

licensee

had recently identified an example of a previous failure to

adequately test primary isolation valve position indication following

implementation of a plant design

change.

WO 97-11249-001

had been

issued to troubleshoot position indication problems for the Unit 3

Drywell- Leak Detection Return Outboard Isolation Valve, 3-FSV-090-0257A.

This condition had been recently discovered during

a fai lure of the

valve to indicate closed during containment isolation valve operability

testing.

During troubleshooting,

licensee

personnel

determined that

valve position indication wiring was

swapped

between

3-FSV-90-255

and 3-

FSV-90-257A.

These valves are the outboard supply and return isolation

valves for the Unit 3 drywell continuous air monitor

(CAM) and are

controlled from a

common handswitch in the Unit 3 Control

Room.

The

licensee

had documented this problem in PER BFPER971786.

The inspectors

reviewed this

PER and noted that the incorrect wiring configuration

had

existed since both valves

had been installed

as part of a design

change

performed during the Unit 3 recovery in 1995.

The apparent

causes

identified in PER BFPER971786 were improper installation

and inadequate

post-modification testing which had not individually tested the valves

and detected

the problem.

The inspectors

concluded that corrective

actions specified in the

PER were adequate

and that required

TS actions

had occurred since the licensee's

actions for 3-FSV-90-257A had been

inoperable.

Also satisfied were

TS requirements

for 3-FSV-90-255

as

being inoperable.

This licensee-identified

and corrected violation is

.being treated

as

a Non-Cited Violation, consistent with Section VII.B.1

of the

NRC Enforcement Policy (Non-Cited Violation 296/97-12-05,

Inadequate

Post Modification Testing).

Conclusion

An NCV was identified for

a previous

example of inadequate

post-

modification testing.

No recent

examples of inadequate

post-

modification testing or post-maintenance

testing were identified.

Improvement

was noted in the licensee's

PMT planning process

on recent

WOs.

Review of Tem orar

Modifications

a.

Ins ection Sco

e

62700

The inspectors

reviewed the licensee's

program for controlling temporary

modifications to permanent plant equipment to determine the adequacy .of

the licensee's

process for review and approval of temporary

modifications

and to verify that any temporary modifications satisfied

requi rements

from Licensee

Procedures

SPP-9.5.

Temporary Alterations,

and SII-O-XX-00-3014, Troubleshooting

and Configuration Control of

Instrumentation.

Observations

and Findin s

The inspectors

reviewed the licensee's

program for control of temporary

modifications to permanent

plant equipment

and determined that these

~

~

16

were controlled through several different methods.

Temporary

modifications of short dur ation were usually controlled in accordance

with

approved plant procedures

such

as testing procedures

or

maintenance

work instructions.

Temporary modifications of longer

duration were controlled in accordance

with SPP-9.5.

Temporary

modifications performed during planned maintenance activities such

as

lifted electrical

leads or installation of temporary jumpers were

controlled in accordance

with SII-O-XX-00-3014.

The inspectors

noted that the licensee's

program required that any

required

10 CFR 50.59 safety assessments

associated

with any temporary

modifications controlled by approved plant procedures

or approved work

instructions would have been satisfied during the procedure or work

instruction review and approval

process.

The inspectors

noted that

temporary modifications to equipment,

which remained out-of- service for

maintenance,

did not requi re performance of a

10 CFR 50.59 safety

assessment.

An'assessment

would have been required for any maintenance

activity that would have required that equipment to have

been placed

back in service with a temporary modification installed.

The inspectors

were informed by licensee

management that this practice

had rarely been

performed

and that for any occurrence

documentation

for the appropriate

10 CFR 50.59 reviews would have been included with the completed work

documentation.

The inspectors

had identified only two examples of

temporary modifications left in place following completion of

maintenance activities during recent

reviews of completed work orders

documented in Section H3.1.

Documentation for both

WOs included the

required

10 CFR 50.59 safety assessments.

The inspectors

also reviewed the licensee's listing of existing

temporary modifications.

The inspectors

concluded that none would

adversely affect the safe operation of Units 2 or 3.

The inspectors

noted that only six active temporary modifications existed for the two

operating units.

The inspectors

determined that licensee controls in each of the above

cases

were adequate to require the appropriate level of review and

approval

for temporary modifications

and to ensure the completion of

required verification steps for proper component

removal

and

reinstallation.

c.

Conclusions

The inspectors

determined that licensee controls were adequate to

requi re the appropriate

level of review and approval for temporary

modifications

and to ensure the completion of requi red verification

steps for proper

component

removal

and reinstallation.

No examples of inadequate

controls of temporary modifications to

ermanent

equipment were identified.

The inspector concluded that the

icensee's

program for controlling temporary modifications was adequate.

17

H7

guality Assur ance in Maintenance Activities

M7. 1

Maintenance/Modifications

De artment Self Assessment

Pro ram

a.

Ins ection Sco

e

62707 92902

One of the resident

inspector s reviewed the Maintenance/Modification

Department self assessment.

program.

The inspector

reviewed Maintenance

Section Instruction Letter HSIL-1. Maintenance Self Assessment

Process,

selected

monthly performance

reports

(September

to December

1997),

and

completed observation checklists.

The inspector discussed

the program

with the Maintenance

Program Coordinator

and the Maintenance

Manager.

The inspector attended

a maintenance

performance evaluation meeting

and

a working level discussion for the Level

1 trend report.

b.

Observations

and Findin s

MSIL-1 provides guidance for the administration of the self assessment

e

rogram.

The program was established

in August 1996.

Table

1 of HSIL-1

ists performance indicators which are used to analyze trends.

The

performance indicators are obtained

or developed

from quality indicators

(such

as

management

reports,

audits,

or

Problem Evaluation Reports)

and

completed observation checklists.

Six checklists

are contained in

HSIL-1 for observation of key maintenance activities.

Table

2 of MSIL-1

assigns

responsibilities

for the checklists

and

a schedule

for

completion.

The following observations

were noted through review of

selected

completed checklists:

The checklists contained in HSIL-1 are highly detailed

and clearly

convey management

expectations

for performance in key areas.

The guidance in Table 2 of HSIL-1 for checklist completions

was

not always being met..

For example.

no MA-1, Management

Overview

checklist was completed for the months of September

and October

1997.

The guidance indicated that at least nine MA-1 checklists

would be completed

each

month.

This checklist is used

by

maintenance

management to assess

observations.

This checklist

appeared to be important regarding maintenance

management

evaluation

and feedback

on the quality of the self assessment

checklists.

The inspector noted that the Maintenance

Manager

completed several of the MA-1 checklists late in December.

1997.

Many of the checklists

completed in September

1997 did not contain

critical comments.

With the exception of several

MA-4.3

checklists which evaluated

planning of work packages,

the

inspector

noted that no checklist items were marked "red"

,(unsatisfactory

performance).

Of a sampling of 25 checklists,

the

inspector

noted only 5 items were marked

as "yellow" (improvement

needed).

~

~

18

~

The inspector

noted that the maintenance

department

as

a group

was initiating less than fifty percent of the.

PERs attributed to

maintenance.

The percentage

was

as high as

80 percent in some

shops but was lower in the Modifications group.

Several

recent

NRC findings in the maintenance

area also are indicative of some

workers not being self critical.

~

The "actions assigned"

section of the checklists

was not being

used.

It appeared that issues

which warranted corrective actions

would be handled through the

PER process.

A significant fraction

of the completed checklists did not contain signatures

for the

individual being observed.

Section 4.3 of MSIL-1 describes

how the

checklist is to be reviewed with the individual immediately after

completion.

Step 4.3.7 indicates that the signature

should be

obtained

acknowledging that feedback

was provided.

~

Maintenance

management

has

been flexible in application of the

self assessment

program.

Area of emphasis

are directed

by

management

as concerns

or problems are identified.

The inspector

noted several

prudent actions

by maintenance

management to address

recognized

weak areas.

For example,

47 checklists

(MA-3, Review of

Work Package)

were completed in September

1997 to address

deficiencies in the area of planning.

The inspector noted that

several of these checklists contained constructive critical

comments.

~

Section 4.2 of MSIL-1 indicates that general

foremen are

responsible for ensuring that the checklists

are completed at the

recommended

frequency.

Discussion with management

indicated that

this responsibility has

been shifted to the maintenance

shop

leads.

Additionally, Section 4.5 indicates that each observation

checklist has

an assigned

owner who is tasked with evaluating

overall performance

and implementing corrective actions.

This

function is actually performed

by the Maintenance

Program

Coordinator.

At the weekly performance evaluation meeting,

the inspector

noted that

performance indicators associated

with areas

recognized

as needing

improvement were emphasized.

The inspector

also observed that the

maintenance

department

was monitoring numerous

performance indicators of

maintenance

proficiency including work efficiency issues.

Using the completed checklists

and the other. quality indicators listed

in MSIL-1, maintenance

management

develops

Monthly Performance

Reports.

MSIL-1 indicates that the Monthly Performance

Reports are used to

develop

a separate

quarterly report.

The actual practice is to use the

monthly reports to develop the. Maintenance

Department input to the

quarterly site Level

1 Trend Report.

The inspector's

review of several

monthly reports indicated that the

monthly reports accurately

summarized the results of completed

checklists.

The monthly reports contained

useful information regarding

19

analysis of the other quality indicators

as well. For example,

the

September

1997 report contained

a detailed review of Problem Evaluation

Reports in the Maintenance/Modifications

area.

The Top Ten

Maintenance/Modifications

Manager's

Issues List addressed

the major

problem areas

noted through the analyses

of the monthly reports.

The

status

and effectiveness

of actions in progress to address

the issues

are specifically addressed

in each monthly report.

The inspector noted that information from the monthly reports

was

effectively incorporated into the June

1997 site Level

1 Trend report:

The trend reports

and the Maintenance/Modification

Manager

Top Ten

Issues appropriately

addressed

regulatory issues

as well as self

identified items.

Review of the open issues

indicates that management

is setting high standards.

For example,

one issue is reduction of

preventive maintenance activities performed within the late band.

Specific items are listed in the action plans to address

each issue.

The licensee

has

been successful

in improving performance in some of'he

areas

noted

as needing

improvement.

For example,

emphasis

on pre-

briefings-and post briefings has increased

the overall quality of

briefings.

The number of significant human performance deficiencies

has

been

reduced in recent

months.

Improvement

has

been noted in some

planning areas.

All of these

issues

have open action plans since

management

is not fully satisfied with performance in those areas.

.The inspector

observed portions of a working group meeting where the

maintenance

department

presented its proposed

input to the January

1998

Level

1 trend report.

The inspector

noted that deficiencies

regarding

scaffolding controls which were the subject of a

NRC violation were not

addressed

during discussion of maintenance

department

procedural

issues.

The representatives

of the other departments

did not question this.

The

inspector observed that the representatives

of the other

departments

were appropriately critical regarding the proposed characterization

of

performance in each area.

c.

Conclusions

Overall, the maintenance

department's self assessment

program has

been

effective in that management

has identified and pursued

areas

needing

improvement.

Numerous maintenance

proficiency indicators are monitored

closely for detection of areas

needing

improvement.

High expectations

are established

through the establishment

of challenging goals.

Performance

data

from completed observation checklists is effectively

incorporated

into monthly reports.

Implementation of the self

assessment

program was prudently revised

by maintenance

management to

focus on recognized

weak areas.

Some of the observation checklists

were noted

as not sufficiently

critical during self assessments.

Several

recent

NRC findings also

indicate that

some maintenance

workers are not being self critical.

H8

H8.1

20

The procedural

guidance for the administration of the self assessment

checklists

does not accurately reflect actual

implementation.

Maintenance

management's

expectations

for feedback to the observed

individual. signatures

on completed checklists,

and degree of self-

critism were not being met.

Enhancement

of the self assessment

program

is included as the first issue

on the Top Ten Maintenance/Modifications

Manager's

Issues

Top Ten Issues list.

Miscellaneous

Maintenance

Issues

(62707,

92902)

Closed

Licensee

Event

Re ort

LER

LER260/97-005-00

ESF

Com onents

Were Actuated

as

a Result of an Inade uate Procedure.

On October

12,

1997,

an inadvertent

engineered

safety features

(ESF) actuation occurred

during post-maintenance

testing of a main steam relief valve

modification during the Unit 2 outage.

Shorting of the circuit, while

jumpers were being placed.

caused

an invalid low level signal which

started all eight emergency diesel

generators,

generated

a Unit 2 full

reactor

scram,

and caused

one loop of core spray to inject into the Unit

2 vessel.=

The inspector's

review of this event is documented

in

inspection report 259,260.296/97-10.

The licensee

documented the root

cause of this event

as

an inadequate

procedure

associated

with the

modification test program.

The procedure did not require

a

performing'nd

support organization

review in the post maintenance test approval

process.

A more conservative test method of jumper installation at

terminal strips rather than at the relay terminal blocks was identified

following the event

and implemented with a change to the test procedure.

The inspector

reviewed the revised Site Standard

Practice

(SSP)

SSP-8.3,

Modification Test Program,

Revision 8, steps

3.4. 1.A. 11 and 3.4.2.A.7,

which included

an independent

review by the support organizations to

ensure that the most appropriate test

methods

are utilized to minimize

the risk of inadvertent

impact on the plant.

Additional corrective

actions included discontinuation of the use of alligator clips on

installed plant equipment without the approval of'he

Maintenance/Modification

Manager.

The inspector

concluded that the

corrective actions adequately

addressed

the apparent

root cause of the

event.

The inspector

reviewed

a previous similar event. that occur red in April

1996, during which all eight

EDGs started.

The inspector

reviewed

inspection report 50-259,260,296/97-09.

which dispositioned the event

as

a Non-Cited Violation for failure to follow a procedure

which required

that revisions to work plans

be sent to planning for review.

Revisions

were made to the work plan to delete the requirement for a

clear ance/isolation

and

a note was added to perform the work "hot".

(energized)

The work plan was never sent

back to planning for review.

The test methodology selected for use in the most recent post

maintenance test was not adequate to preclude

an inadvertent

engineered

safety features

actuation.

The inspector concluded this was not

a

violation that could reasonably

have been prevented

by the licensee's

'orrective actions for the discussed

previous violation. This non-

'

21

repetitive licensee identified and corrected violation is being treated

as

a Non-Cited Violation (NCV), consistent with Section VII.B.1 of the

NRC Enforcement Policy.

(NCV 50-260/97-12-03.

Inadequate

Procedure for

PMT)

Closed

Licensee

Event

Re ort

LER 260/96-005-00

Unit 2 Scrammed

on

Low Reactor

Water

Level

Due to the Digital Feedwater

System

Reinitializing its Feed

Pump

Demand Output Signal to Zero and the

Subsequent

Trip of the Reactor

Core Isolation Cooling on High Exhaust

Pressure.

Inspection

Report 259,260.296/96-05

addressed

details of the

Unit 2 scram

and subsequent

reactor

core isolation cooling

(RCIC) system

trip following initiation.

Related

enforcement

actions are documented

in a subsequent

letter and Notice of Violation issued August 1,

1996.

The licensee

documented

a specific commitment in the

LER to strengthen

procedural

requi rements for the inservice testing program with regard to

control of testing activities.

The inspector verified that Site

Standard

Practice

SSP-8.3,

Modification Test Program,

Revision 8,

included enhancements

to the Retest

Control

Form to state the basis for

specifying the test.

This

LER is closed.

Cl osed

Violati on 260/96-199-01013

RCIC Inoperabi

1 ity.

Thi s violati on

is addressed

in the Notice of Violation transmitted

by a letter dated

August 1,

1996,

from the

NRC to TVA.

This violation involved the

inoperability of the Unit 2 RCIC system for a period greater

than that

allowed by Technical Specifications

(TS).

RCIC was returned to a fully

operable status

by implementing

a design

change which raised the

RCIC

exhaust

pressure trip setpoint from 25 psig to 50 psig.

This change

was

previously reviewed by the resident inspectors

and documented in NRC

IR 259.260,296/96-05.

Corrective actions

were inspected in conjunction

with those described in Section M8.2.

The inspector additionally

verified that Quality Assurance

performed the independent

assessment

of

the corrective actions within six months of the licensee's

submittal

as

discussed

in the licensee's

response.

This violation is closed.

Closed

Violation 260/96-199-02014

Failure to Comply with IST

Requirements.

This violation involved two examples of failure to

perform required American Society of Mechanical

Engineers

(ASME)

Section

XI in-service testing (IST).

Both the

RCIC system turbine

exhaust

check valve and the

HPCI system turbine exhaust

check valve were

returned to service after having undergone

maintenance

(replacement)

without adequate

IST being performed

on the valves.

Quality Assurance

evaluated

the effectiveness

of the licensee's

corrective actions

and

concluded that the corrective actions

were effectively implemented.

The

inspector

reviewed the

QA evaluation

and noted that the licensee

included the use of techniques

such

as interviews

and database

searches

to acquire data to support their conclusion.

The inspector verified

that

ASME Section

XI training was performed for Technical

Support

Engineers in September

1996.

as documented

in BFPER960710.

This

violation is closed.

El

Conduct of Engineering

22

III. En ineerin

E1.1

Control Air S stem Transients

and Air ualit

Ins ection Sco

e

37551

The inspector

reviewed the licensee's

corrective actions to address

several

incidents in which control air system pressure

decreased

significantly below the normal operating pressure.

The inspector

also

verified that measures

were in place to ensure that air quality

requi rements

are periodically tested.

b.

Observations

and Findin s

The control,air system supplies air pressure to various control systems

and to the control rod drive hydraulic system.

An automatic reactor scram will occur if control air pressure

lowers to a predetermined

level.

Small reductions in control air pressure

were experienced

on

several

instances

in the November

1997 time frame on Unit 2.

The

transients

were determined to be caused

by actuation of the excess

flow

check valve on the inlet of the control air dryers supplying air at that

time (Unit 2 or Standby).

This valve actuates

to shut off flow to the

.dryer,

and therefore the control air system,

when excess

flow to the

dryer is

experienced.'nitial

troubleshooting efforts focused

on system leakage

downstream of

the dryers

and improper operation the excess

flow check valves.

Later,

the licensee

determined that the excess

flow check valves were actuating

due to degraded

conditions of the control air dryers.

Solenoid

and

check valves which transfer flow through the two dryer desiccant

towers

(one on line and one in a dessicant

regenerative

mode) were found to be

excessively

worn.

The results of these

degraded

conditions resulted in

increased

flow to the control air dryer which actuated

the excess

flow

check valves.

The licensee

determined that the root cause of the degraded

conditions

of the dryers

was due to a lack of preventive maintenance.

Corrective

actions included performing preventive maintenance

on flow transfer

components

on

a regular schedule.

Increased

moisture

has also been observed

on the Units 2 and 3 control

dryer inlet prefi lters.

The system engineer indicated that this was due

to the installation of a higher capacity control air compressor

which

has

a lower capability of moisture

removal than the original

compressors/moisture

separators.

This resulted in an operator

work

around which required the blowdown of the control air dryer prefilter

on

a regular basis.

A design

change

has

been partially completed which

installed water traps

on the control air dryer prefilters.

However,

problems with the installation of the drain lines (insufficient line

slope)

has delayed their being put into operation

and has resulted in

V

E8

23

continued operator

work arounds to regularly blow down the water traps.

The licensee is currently reviewing options to the drain line slope

problems.

The inspector verified that the licensee

had measures

in place to verify

control air/instrument air quality.

The inspector

found that O-TI-34,

Monthly Control Air System Dryer Dewpoint Test and Purge Control,

performs moisture content .checks

on control air dryer and drywell

control air systems.

0-TI-173. Control Air Sampling, periodically

(every

6 months) performs air particulate

and hydrocarbon

checks

on

these

systems.

These preventive maintenance

items are performed based

on the licensee's

commitments

made in response to

NRC Generic Letter 88-14.

Conclusion

The licensee

has

implemented significant modifications to increase

the

air system capacity

and reliability.

Insufficient preventive

maintenance

on the control air dryers resulted in several

air system

transients.

Problems with the installation of water trap drain lines

has resulted in operator work around which the licensee is continuing to

resolve.

The licensee is periodically monitoring control/instrument air

quality as documented in the response to Generic Letter 88-14.

.Miscellaneous

Engineering

Issues

(92903)

E8. 1,

Closed

Licensee

Event

Re ort

LER 259/97-004-00

Residual

Heat

Removal Service Water

Pum

Limitin Condition for 0 eration is Non-

Conservative.

The

LER documented

an inconsistency

between

statements

in

the Updated Final Safety Analysis Report

(UFSAR) and Technical Specification 3.5.C,

regarding the number of Residual

Heat

Removal

Service Water

(RHRSW) pumps required to remove heat from a unit

following a design basis accident.

The

UFSAR states that within one

hour following a design basis accident, six RHRSW pumps will be required

to supply cooling water to the

RHR heat exchangers.

The licensee

has

determined that two RHRSW pumps

per unit are required to serve the core

and containment cooling function following a design basis accident.

The

current

TS requires

seven, five, or four pumps to be operable

and

assigned to

RHRSW service with three,

two,

and one units fueled,

respectively.

Since two RHRSW pumps are supplied from emergency diesel

generator

A and two are supplied from emergency diesel

generator

B, then

the potential existed for

a single failure of diesel

generator

A or

B to

reduce the number of available

pumps to less than the number of pumps

described in the

UFSAR for the case of two or three unit operation.

The licensee

completed

an analysis to determine the suppression

pool

temperature

response

for the non-accident unit-following a loss of

coolant accident or other design basis accident in the opposite unit.

considering

a complete loss of offsite power and the worst case single

failure.

The analysis

supported the licensee's

conclusion,

as presented

in the

LER. that more than two hours is available to the operators

for

either restoring another

RHRSW pump to service or for establishing

't e~

gpss

24

alternate

power to the two RHRSW pumps lost as

a result of the single

failure.

The inspectors

reviewed the Emergency Operating Instructions

and verified that procedures

prompted the operators to 'initiate

suppression

pool cooling.

The inspector discussed this issue with

control

room

Senior Reactor Operators

who indicated that actions would

be taken to restore

power to the 4kV shutdown board through the crosstie

to the appropriate

EDG on the other unit.

The inspector

reviewed

O-AOI-57-1A, Loss of Offsite Power

(161 and 500 kV) / Station Blackout,

to verify that instructions were provided to 'operators to energize

a

Unit 1/2 4kV shutdown board using

a Unit 3 diesel generator.

The

licensee

concluded that the condition described

by this event would not

degrade

the

RHRSW safety function to an extent that would prevent

a unit

shutdown.

The inspectors

noted that the licensee

event report

assessment

of safety consequences

sufficiently detailed the licensee's

analysis

and conclusions.

The assessment

was improved from previous

examples

documented

by the inspectors.

The licensee's

corrective actions

included administrative controls to

ensure that the four RHRSW pumps would be available after

a single

failure during two unit operation.

The inspector verified that

Operating Instruction O-OI-23, Residual

Heat

Removal Service Water

System,

was changed to require that either six RHRSW pumps are required

for two fueled units or if only five RHRSW pumps are available,

they

shall

be powered from five separate

4kV Shutdown Boards.

The licensee

also submitted

a Technical Specification

(TS) change to the

NRC on

December

30,

1997, to correct the non-conservative

TS.

This issue represents

a failure to assure that the design basis

was

correctly translated into specifications.

drawings,

procedures

and

instructions.

The licensee identified this issue,

performed

a thorough

assessment

of the safety implications,

and initiated corrective actions.

The licensee's

evaluation adequately

supported the conclusion that this

deficiency would not have prevented

a safety system from performing its

function under

design basis accident conditions.

This licensee-

identified and corrected violation is being treated

as

a Non-Cited

Violation. consistent with Section VII.B.1 of the

NRC Enforcement

Policy.

(NCV 259.260,296/97-12-04,

Design Basis

Not Translated

Properly

for RHRSW Pump Requirements)

Closed

Ins ection Followu

Item

IFI

260 296/95-064-10

Secondar

Containment Ventilation Dam er Failures.

This issue

was previously

discussed

in NRC inspection reports 259.260,296/95-64

and

259,260,296/96-08.

The issue involved secondary

containment ventilation

damper failures due to sticking solenoid valves.

The solenoid valve

sticking was suspected

to be occurring at the core-plugnut interface.

The inspector attended

the Maintenance

Rule

(MR) Expert Panel

meeting

on

January

8,

1998. which reclassified the Secondary

Containment Isolation

System from MR a(l) status to

MR a(2) status.

The members

discussed

that all the associated

solenoid valves

had been replaced

by February

1997 and no associated

solenoid valve problems

have occurred since the

replacement.

The discussion

indicated that in July 1997, the licensee

ended weekly swapping of the fans, currently the fans are

swapped

every

E8.3

E8.4

25

six weeks.

The licensee

had approximately six months of "typical

operation" data without an associated

solenoid valve failure.

The

system engineer

considered that the problem was resolved with the

changeout of solenoid valves.

As discussed

in Section El. 1 of this

report, the resident

inspectors

also verified that control air quality

is being monitored.

The lack of failures

on the secondary

containment

ventilation

dampers

indicates that the specific system problem

resolution

was adequate.

This IFI is closed.

Closed

Ins ection Follow-U

IFI

260/97-05-04.

Spurious

Main Steam

Isolation Valve (MSIV) Closure

on Reactor

Scram.

Sections

E1.2 and Ml. 1

of NRC Inspection Report 97-10 describe detailed review of modification

activities completed to reduce the probability that the MSIVs would shut

unnecessarily

following a reactor

scram.

A minor problem with the

capacitor

calculation

was identified.

Overall implementation

and design

was adequate to address

the problem.

The IFI is closed.

Closed

Licensee

Event

Re ort

LER 260/96-007,

Unit 2 Scram

on Turbine

Control Valve Fast Closure

Due to Loss of Excitation to Main Generator.

NRC Inspection Report 96-12 describes

NRC review of the event.

The

event was attributed to an incorrectly revised maintenance

procedure for

main generator

exciter bush replacement.

The corrective actions listed

in the

LER were completed.

The resident

inspectors verified that the

event

had been correctly characterized

as

a preventable failure in the

.maintenance

rule program.

The

LER is closed.

P2

P2.1

IV. Plant

Su

ort

Status of Emergency Preparedness

(EP) Facilities,

Equipment,

and

Resources

Ins ection Sco

e

82701

This area

was inspected to determine whether the licensee's

Emergency

Response Facilities

(ERFs)

and equipment

were adequately

maintained in

accordance

with the Emergency

Plan.

Requirements

applicable to this area

are found in 10 CFR 50.47(b)(8)

and (9),

10 CFR 50.54(q),

Sections

IV.E

and VI of Appendix

E to 10 CFR Part 50,

and the licensee's

Emergency

Plan.

Observations

and Findin s

The inspector toured the Technical

Support Center

(TSC) and Operational

Support Center

(OSC)

and tested telephones.

fax machines,

and

Emergency

Response Facility Information System monitors

and Computers.

All

equipment tested satisfactorily.

The inspector

reviewed several

controlled volumes of the Emergency

Plan Implementing Procedures

(EPIPs) in the

ERFs for being

maintained

up to date.

All of the EPIPs

reviewed were up-to-date.