ML18038B918

From kanterella
Jump to navigation Jump to search
Insp Repts 50-259/97-07,50-260/97-07 & 50-296/97-07 on 970511-0621.Violations Noted.Major Areas Inspected: Operations,Engineering,Maintenance & Plant Support
ML18038B918
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 07/17/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18038B919 List:
References
50-259-97-07, 50-259-97-7, 50-260-97-07, 50-260-97-7, 50-296-97-07, 50-296-97-7, NUDOCS 9707250142
Download: ML18038B918 (56)


See also: IR 05000259/1997007

Text

U.S.

NUCLEAR REGULATORY COMMISSION

REGION II

Docket .Nos:

License Nos:

50-259,

50-260,

50-296

DPR-33,

DPR-52,

DPR-68

Report Nos:

50-259/97-07,

50-260/97-07,

50-296/97-07

Licensee:

Tennessee

Valley Authority

Facil.ity:

Browns Ferry Nuclear Plant, Units 1,

2 & 3

Location:

Corner .of Shaw and Browns Ferry Roads

Athens,

AL

35611

Dates.

May 11

- June 21,

1997

Inspectors:

Approved by:

L. Wert, Senior

Resident

Inspector

M. Morgan, Resident

Inspector

J. Starefos,

Resident

Inspector

M. Lesser,

Chief

Reactor Projects

Branch

6

Division of Reactor Projects

Enclosure

2

9707250i42 9707i7

PDR

ADOCK 05000259

8

PDR

0

0

EXECUTIVE SUMMARY

Browns Fer ry.Nuclear Plant, Units 1,

2

8 3

NRC Inspection Report 50-259/97-07,

50-260/97-07,

50-296/97-07

This integrated

inspection included aspects of licensee operations,

engineering,

maintenance,

and,plant support.

The report covers

a six-week

period of resident inspection.

0 erations

NRC inspectors identified that controls

on emergency operating instruction

(EOI) ladders

were not sufficient to ensure that ladders

remained available.

The ladder found at one station

was not sufficient to complete

an emergency

operating instruction task.

The ladders

were not controlled as strongly as

other emergency operating instruction tools.

The inspectors

concluded that

the extensive corrective actions listed in section 01.1 adequately

addressed

the violation and the underlying deficiencies.

The licensee significantly

improved controls on EOI ladders.

(Violation 260,296/97-07-01,

EOI Ladders

Not

Adequately Controlled, Section 01.1)

The licensee's

recent revision of Assistant Unit Operator

(AUO) work

assignments

is a good initiative.

During this period, only a very few

deficient equipment conditions were noted that had not been identified during

AUO rounds.

In addition to the good performance

noted involving an electro-

hydraulic fluid leak, several

other examples

were noted during this report

period in which AUOs identified and reported minor deficiencies.

(Section

02')

Haintenance

Overall conduct of Common Accident Signal testing

was good.

Workers were

particularly cautious regarding

component identification.

The prebriefing was

good, appropriate

issues

were highlighted by the supervisors.

The Test

Director was very important to the successful

implementation of the testing.

Hinor deficiencies involving documentation of step completion

and labeling

issues

are being addressed

by the licensee.

(Section Hl.l)

The inspector

concluded that the licensee

had implemented

good maintenance

controls over the installation of temporary cover s over the spent fuel pools.

(Section Hl.2)

NRC inspectors identified several

examples in which'Foreign Haterial Exclusion

administrative controls were not implemented properly.

No actual

instances of

foreign material introduction were identified.

Although overall

FHE controls

have been strengthened

since

1995, these deficiencies indicate that the

implementation of FHE .administrative controls is not consistent.

(Violation

260,296/97-07-02,

Foreign Haterial Exclusion Controls not Implemented in

Accordance with Procedures,

Section H1.3)

O~

il

il~

A review of a sampling of Inservice Test data indicated that the current

implementation of the program requirements

is adequate.

The licensee is

conducting appropriate monitoring of safety system valve and

pump operability.

(Section H1.4)

Review of the on-going Fire Protection piping replacement

and repair program

is adequate.

Overall, the licensee

has initiated significant actions,

including chemical treatment,

which have improved the overall reliability of

the

FP suppression

systems.

(Section H2.1)

An isolated

case

was identified in which the review for a planned voluntary

entry into a Technical Specification Limiting Condition for Operation

(LCO)

was not thorough.

Licensee

management

expectations

for planning regarding

entry into LCOs for modification work were not met.

The equipment

was not

actually removed from service

and corrective actions

were initiated

immediately.

The licensee

intends to revise procedural

guidance regarding

control of voluntary entry into LCOs.

(Section H3.1)

En ineerin

The licensee

has initiated actions to address

inaccuracies

in the calculations

for spent fuel pool temperature identified during the most recent refueling

outage.

No actual

adverse affects

on important plant equipment

were noted.

Additional review of the licensee's

practices

and the Updated Final Safety

Analysis Report descriptions of spent fuel pool cooling system capacity is

warranted.

(Inspection Followup Item 260,296/97-07-03,

Spent

Fuel

Pool

Cooling System

Heat Removal Capability, Section El.l)

Although engineering

personnel

pursued corrective actions to address

the

postulated

cause of an earlier spent fuel pool cooling pump problem,

a Problem

Evaluation Report was not initiated,

and plant management

was not informed of

the runout problem.

Subsequently,

the

pump failed.

The control

room

operators'ctions

following indications of pump failure did not meet

management

expectations.

Additional

NRC review of this issue will be

conducted

when more information is available

(Unresolved

Item 260/97-07-04,

Failure of Fuel

Pool Cooling Pump, Section E2.1).

Plant

Su

ort

Walkdowns of the protected

area security fencing and inspections of the

Central Alarm Station

and the Secondary

Alarm Station identified no

significant deficiencies.

Security personnel

in the alarm stations

were alert

and attentive to their duties.

(Section S2.1)

V

0

Re rt Details

Summar

of Plant Status.

Unit 1 remained in a long-term lay-up condition with the reactor defueled.

Unit 2 operated at or near full power with the exception of'outine testing

and scheduled

maintenance

downpowers

and the following power reduction.

On

Hay 22, at approximately.9:00

p.m.,

CDT,

an electro-hydraulic control

(EHC)

oil leak occurred

on the servo valve for the

number.

2 turbine control valve.

Power was reduced to 70 percent rated thermal

power, the leak was isolated,

and the servo was replaced.

Power

was restored to full rated

power on Hay 23.

Unit 3 operated

at or near full power during the report period with the

exception of routine testing

and scheduled

maintenance

downpowers.

While performing the inspections

discussed

in this report, the inspectors

reviewed the applicable portions of the Updated Final Safety Analysis Report

(UFSAR) that related to most of the areas

inspected.

Section El.l describes

a

review relating to spent fuel pool cooling system capacity during refueling

outages.

An Inspection Followup Item was identified since additional

NRC

review is necessary

to ensure that the

UFSAR description accurately reflects

the licensee's

actual practices.

I.

rations

01

Conduct of Operations

01.1

Emer enc

0 eratin

Instruction Ladders

a.

Ins ection Sco

e

71707

On Hay 27,

1997, while performing a walkdown of the Unit 3 Reactor

Core

Isolation Cooling System,

the inspectors

noted that

an Emergency

Operating Instruction (EOI) ladder was not in its designated

ladder

storage station in the Unit 3 Reactor Building 541'levation.

The

inspectors

subsequently

examined the controls associated

with EOI

ladders throughout the plant.

b.

Observations

and Findin s

On Hay 27,

1997, while performing

a walkdown of the Unit 3 Reactor

Core

Isolation Cooling System,

the inspector noted that the Emergency

Operating Instruction (EOI) ladder

3-RB-541-1, which is required to

perform specific EOI appendix actions

was not in its designated

hanger.

The inspector

noted that

a ladder was available for use in the area

and

that

a scaffold was in place for work in the area

where the ladder would

be needed.

0

The inspector subsequently

examined

EOI Inventory Form No. 0-EOI-000-

0010,

EOI Ladder Stations

(Unit 2/3) which is Attachment

15.22 of

General

Operating Instruction O-GOI-300-1, Operations

Routine Sheets.

The inspector

determined that discrepancies

existed regarding

two of the

eleven

adders

on the inventory form.

The form required

a

10 ft

extension

ladder at ladder station 3-T8-565-1, but

a 10 ft step ladder

'as

found at the location.

A 10 ft step ladder

was also found at ladder

station 3-RB-565-1 which required

a 20 ft extension ladder.

The

licensee

was informed of the problem and promptly initiated

a problem

evaluation report

(PER).

On June

12,

1997, the inspectors

sampled

EOI Appendix actions to

determine if the

10 ft step ladders

would have

been acceptable

to

perform required valve manipulations.

The 10 ft step ladder

which was

previously found in ladder station 3-RB-565-1 was determined to be

inadequate

for performance of 3-EOI APPENDIX-7J, Alternate

RPV [Reactor

Pressure

Vessel] Injection System Lineup HPCI [High Pressure

Coolant

Injection] Using Auxiliary Steam,

Revision 0, step 9c which requires

dispatched

personnel

to slowly open 3-SHV-012-0798,

RB HPCI SOY.

During the June

12 walkdown, the inspectors

also identified three valves

which were addressed

in the

EOI Appendices which did not have

EOI tags

on the valves.

(These

EOI tags are orange labels

used to facilitate EOI

component identification, valve identification labels were in place.)

The licensee

promptly placed

EOI tags

on the identified valves.

In

addition, the inspectors

reviewed

a draft revision to 0-GOI-300-1

Attachment 15.22 to verify that

a sample of the described

ladders

were

in place.

The inspectors

found that

adder station 2-TB-565-1 had

a

16 ft ladder in place instead of the 20 ft ladder described

by

Attachment 15.22.

The licensee

was informed and promptly placed

a 20 ft

ladder in ladder station 2-TB-565-1.

Although a 20 ft ladder

was more

appropriate,

the inspectors

determined that

a 16 ft. ladder would not

have

been inadequate.

General

Operating Instruction O-GOI-300-1, Operations

Routine Sheets,

Attachment 15.22,

EOI [Emergency Operating Instruction] Tools and

Equipment Inventory Checklist,

dated

May 5,

1997, states that ladders

are secured with GGHKA padlocks at the designated

EOI ladder stations.

Included in Attachment 15.22 is EOI Inventory Form 0-EOI-000-0010

EOI

Ladder Stations

(Unit 2/3) which describes,

in part,

a 20 ft Extension

Ladder, in place

and padlocked,

at ladder station 3-RB-565-1, Reactor

Building Elevation 565'.

The inspectors

noted that

EOI ladders

were not as rigidly controlled as

other

designated

EOI tools.

The licensee

also permitted

EOI ladders to

be used for other purposes.

The failure to adequately establish written procedures for EOI ladder

station control

as identified on Hay 27,

1997,

when the required

20 ft

extension

ladder

was not in place

and padlocked in ladder station

3-RB-565-1 is identified as Violation 50-260,296/97-07-01,

EOI Ladders

Not Adequately Controlled.

il~

0

0

The following is

a list of many of the licensee's

corrective actions

as

identified in Problem Evaluation Report

(PER)'FPER970889:

The ladder at ladder station 3-RB-541-1 was returned to proper

location by on-shift Operations

personnel.

This item was completed

Hay 2,

1997.

An item'as

added to Operations Daily Instructions,

reminding on-

shift Operations

personnel

EOI ladder

usage .is to be restrained

to

EOI use only.

This item was completed

Hay 28,

1997.

All EOI ladders,

as addressed

in Procedure

O-GOI-300-1,

Attachment 15.22,

were verified in place, properly stored,

padlocked,

and

a numbered

EOI seal

was placed

on the lock hasp.

This action was completed

June 4, 1997.

A walkdown audit of all Unit 2 and Unit 3 EOI appendices

was

performed by BFN Operations

Support.

This audit field-verified

in-plant component manipulations with the potential

for ladder

use.

This action was completed

June 4,

1997;

One ladder,

Ladder Station 2-RB-565-1 was found to contain

a

24 foot ladder vice a 20 foot ladder

(referenced

as

a

10 foot

extension)

~

The 24 foot ladder

was deemed to be more appropriate.

O-GOI-300-1, Attachment 15.22 will be revised to reference

the

24 foot ladder at this station.

This action was completed with

O-GOI-300-1, Revision 44, issued

June 6,

1997.

The walkdown determined

no new ladders

were required.

This action

was completed

June 4,

1997.

All ladders

had

new signs placed

on the wall at each station,

signifying "FOR EOI

USE ONLY."

These signs were incorporated into

the licensee's

Permanent

Information Posting

(PIP) program

and

will be audited

as part of that program. This action was completed

June 5,

1997.

All ladders

were individually labeled with orange

EOI labels which

were also

added to the PIP program.

This action was completed

June 5,

1997.

O-GOI-300-1, Attachment 15.22 will be revised to include corrected

information identified during walkdowns

and added

EOI seal

number

to audit.

This action was completed with O-GOI-300-1,

Revision 44, issued

June

13,

1997..

Operations

revised all affected Unit 2 and Unit 3 EOI appendices

to reference the potential

use of a ladder for appropriate

steps

and to include designated

ladder in Tools and Equipment Attachment

in each associated

appendix.

This action was completed

June 23,

1997.

0

0

C.

Conclusions

NRC inspectors identified that written procedures

were not adequately

established

to ensure control of EOI ladders.

The inspectors

concluded

that the extensive

and expedient corrective actions listed in. this

section adequately

addressed

the violation and the underlying

'eficiencies.

Controls were significantly improved for EOI ladders.

EOI ladders will be treated similar to other

EOI equipment

and

will

only be used for

EOI purposes.

02

Operational

Status of Facilities and Equipment

02.1

Reactor

Core Isolation Coolin

RCIC

S stem Walkdown

a.

Ins ection Sco

e

71707

The inspector

conducted

an. inspection of the operational

status of the

Unit 2 and Unit 3 Reactor

Core Isolation Cooling (RCIC) Systems.

b.

Observations

and Findin s

On Hay 28,

1997, the inspector performed

a review of the control

room

position indication for selected significant, valves in the Units 2 and 3

Reactor

Core Isolation Cooling (RCIC) Systems.

The inspectors

also

performed walkdowns of portions of the RCIC systems

on both units.

The

inspector

noted that an Emergency Operating Instruction (EOI) ladder was

not in its designated

ladder storage

station in the Unit 3 Reactor

Building 541'levation

as discussed

in Section 01.1 of this report.

In addition, the inspector performed'

review of outstanding

work order s

on the Unit 2 RCIC system.

The inspector did not identify any

inappropriately delayed maintenance

issues or other problems.

The inspector also verified that

a procedure

step to locally exercise

the RCIC turbine control valve by depressing

the servo approximately

2 inches to ensure

no binding of the control valve stem had been

removed

from Surveillance Instruction (SI) 2/3-SI-4.5.F.1.d,

RCIC System Rated

Flow at Normal Operating Pressure.

The step

was removed from the Unit 2

procedure with the issuance of Revision 27 effective 3/25/97

and from

the Unit 3 procedure with the issuance of Revision 7 effective 3/31/97.

02.2

E ui ment Condition and Watchstandin

Activities

a.

Ins ection Sco

e

71707

The inspectors

examined the condition of important plant equipment

during tours of the plant.

One of the inspectors

also obser ved an

Assistant Unit Operator

(AUO) perform daily rounds of the Unit 3 Reactor

and Turbine Buildings..

0

b.

Observations

and Findin s

On June

12,

1997., the inspector observed

performance of technical

instruction O-TI-165A, Appendix

R Backup Control Test for EECW, section

7.3,

0-FCV-67-22 Test.

The inspector

observed the Assistant Unit

Operator perform several

steps at the breaker

compartment

and noted that

the operator verified the correct components prior to performance of the

action.

The inspector also observed

an independent verification step

and

a second party verification step which were accomplished

in

accordance

with the licensee's verification program.

On June

14,

1997, the inspector

observed

an Assistant Unit Operator

(AUO) perform daily rounds of the Unit 3 Reactor

and Turbine Buildings.

The AUO identified and addressed

discrepancies

appropriately.

As

discussed

in NRC Inspection Report 50-259,260,296/97-05,

the licensee

has recently revised work assignments

to the AUOs with the intent to

reduce interruptions to AUOs while on plant tours

and improve the

effectiveness of the rounds.

Currently one

AUO is assigned to perform

Reactor Building and Turbine Building rounds while another

AUO is

designated

as support.

During the rounds observed

on June

14,

1997, the

inspector

noted that only a single request

was

made of the rounds

AUO

which was outside of his assigned

rounds duties.

On Hay 25,

one of'he inspectors

noted that the "A" train Standby

Gas

Treatment

(SBGT) System backdraft

damper

was stuck open.

A 1996 work

request tag for lubrication was attached to the damper.

Apparently, the

damper

had not shut after the train was operated the previous day.

Operations shift management

reported to the inspector that the damper

condition did not adversely affect train operability.

The inspector

noted that the damper condition had not been identified by Operations

personnel

during rounds.

Additionally, the inspector

noted that the Continuous Air Honitor (CAN)

located near the "A" SBGT system

had

a Work Request tag dated February

14,

1997, attached.

The tag stated

"CAN not counting correctly."

The

inspector

conducted additional

review since the tag implied that the

CAH

may be inoperable.

Radiological Controls personnel

consider ed the

CAH

to be operable

since the routine functional test

was completed

satisfactorily.

The inspector subsequently

determined that

a problem in

the

CAN calibration procedure

had resulted in the generation of the work

request

and the

CAH was actually operable.

A Problem Evaluation Report

had been previously initiated to address

the calibration procedure

problem and was modified to included this specific CAN.

The inspector

noted that the calibration procedure did not require that the workers

notify Radiological Controls personnel

when the

CAH could not be

calibrated.

The inspectors

noted that an Electro-Hydraulic

(EHC) fluid leak that

occurred

on the Unit 2 number

2 turbine control valve on Nay 22 was

handled well.

During rounds, the

AUO noted that the

EHC reservoir

level

had. decreased

unexpectedly

and notified the control

room.

Shortly

thereafter,

the low level annunciator

alarmed.

The alarm response

ik

08.1

procedures

were implemented.

Good teamwork between the various work

groups resulted in the source of the leak being identified, isolated,

and repaired very quickly.

Conclusions

The inspectors

concluded that,

although not all deficient conditions

were identified by AUOs during rounds,

the licensee's

recent revision of

AUO work assignments

is

a good initiative.

In addition to the good

performance

noted involving the

EHC leak,

several

other

examples

were

noted during this report period in which AUOs identified and reported

deficient or questionable

conditions.

Hiscellaneous

Operations

Issues

(92901)

Withdrawn

Violation 260/94-14-01

Inadequate

Procedure Controlling

Voluntary Technical Specification

(TS) Limiting Condition for Operation

(LCO) Entries.

This violation addressed

an incident in which the

onshift Shift Technical Advisor (STA) identified that planning efforts

for modification work involving the

3D emergency diesel

generator

had

not addressed

affects

on standby coolant supply from the Bl and

B2

residual

heat

removal service water

(RHRSW) pumps.

The TS

LCO for

standby coolant

(30 days)

had not been entered until about five hours

after the

EDG was removed from service.

The licensee

responded to the violation on July 28,

1994, with a

position that

a violation did not occur .

The licensee did not contest

the underlying issues'ut

stated that the incident involved

noncompliance with a verbal

commitment

made at

a TVA/NRC meeting

on

Hay 10,

1994.

At that meeting,

TVA presented

plans for controlling

Unit 3 recovery activities that would require entry into a Unit 2 TS

LCO.

In an August 26,

1994, letter to TVA, NRC withdrew the violation.

The

letter stated that since the commitment involving the Unit 2

LCO entries

due to Unit 3 work was not

a formal written commitment,

a notice of

deviation will not be issued.

Because

the Unit 3 restart is complete,

many aspects of this issue are

.

no longer pertinent at Browns Ferry.

Section

H3.1 of this report

describes

NRC inspection of TS

LCO entries for any modification work

(not just operating unit affected by restart of a shutdown unit) which

are related to this incident.

Additionally, as described in Inspection

Report 259,260,296/97-04,

detailed

NRC review of the licensee's

controls

over removal of plant equipment

from service

was recently performed.

0

II. Haintenance

H1

Hl.l

a.

b.

Conduct of Haintenance

Survei11ance

Testin

of Unit 1 and Unit 2 Common Accident Si nal

CAS

~Lo

1C

Ins ection Sco

e

61726:

The inspectors

monitored the performance of portions of Surveillance

Instruction 1/2-SI-4.9.A.3.a,

Common Accident Signal Logic.

This is a

complex surveillance

which requires several shifts and coordination

between

numerous

workers to complete.

One of the inspectors directly

observed

most of the Division I testing.

Operation of the emergency

diesel

generators

(EDGs) in accordance

with Operating Instruction OI-82,

was observed.

The completed procedure

was reviewed.

The inspectors

also

reviewed applicable plant drawings,

the

UFSAR,

and TS to verify that

selected plant equipment

was adequately

addressed

by the testing.

Observations

and Findin s

The inspector noted that the pre-briefing for the testing was good.

Communication issues,

self checking,

and correct second party checking

wer e emphasized

several

times during the briefing.

Deficiencies during

previous testing were also discussed.

It was emphasized that the

testing included operation of equipment in different units.

The test

director clearly explained expectations

during the testing.

During the observed division I testing. the inspector

noted that workers

were cautious regarding correct

component identification and self

checking.

Several

examples

were noted in which the equipment label did

not match the wording used in the test procedure.

In at least

one case,

the workers stopped the test

and requested

additional

guidance to ensure

the correct

component

had been identified. There were more than 30

validation comments submitted by the test personnel.

The Test Director

was instrumental

in ensuring proper coordinatson

between the different work groups

and locations during the test.

The

inspector observed that the director was very familiar with the test

procedure

and equipment involved.

The inspectors

observed

some of the

EDG operations

conducted

as part of

the test.

It was noted that one

AUO did not verify that the

EDG

electrical control cabinet exhaust

fan was running.

Subsequent

discussion with the system engineer indicated that proper

operation of

the fans is important to prevent failures in the cabinet

due to

excessive

heat.

The inspectors

informed Operations

management that the

check was not properly performed by the AUO.

0

The inspector

noted that alligator clips were used in several

applications during the test.

Although the workers were careful to

fully attach the clips, this is not

a good practice.

In several

sections of this test,

an alligator clip slipping off of a contact could

have significant effects

such

as

an inadvertent

engineered

safety

features

actuation.

Operating personnel

donned the protective clothing required by General

Operating Instruction 300-2, Electrical,

when racking the 4160V shutdown

board

br eakers to the "test" position.

On several

portions of the test,

the sign off for completion of one step

was not always completed prior to performance of another step.

An

example would be booting several

contacts in a particular re'lay.

Workers would identify the relay,

mark it with orange tape

as expected,

and carefully perform the listed actions. After the steps

associated

with the specific relay were completed,

the workers would sign the

individual steps.

The inspector

noted that the test director was

careful to ensure that each step was, in fact, completed prior to

proceeding.

This practice

has

been observed during other surveillance

tests

and licensee

management

is reviewing the guidance currently set

forth in SSP-2.1,

Site Procedures

Program for signing off steps of

continuous

use procedures.

Revision of some continuous

use procedures

may be appropriate

so that successful

performance of steps is not

impacted by stopping to sign steps.

The inspectors

selected

several

portions of the

common accident

circuitry and verified that the test adequately

addressed

the entire

circuit.

In some cases,

relays

used to actuate portions of the

circuitry are tested

by other test procedures.

The inspectors verified

that those procedures

addressed

the specific relays required.

The

inspectors

also examined the functioning of the

common and pre-accident

circuitry in regards to the

UFSAR descriptions

and drawings.

The

completed test procedure

was reviewed.

No deficiencies

were identified.

Conclusions

Overall conduct of the testing was good.

Workers were particularly

cautious regarding

component identification.

The prebriefing was good

and appropriate

issues

were highlighted by the supervisors.

The

inspector

concluded that the Test Director

was very important to the

successful

implementation of the testing.

Hinor deficiencies involving

documentation of step completion

and labeling issues

are being addressed

by the licensee.

The large

number of validation comments indicate that

worker s are making efforts to improve the quality of the procedure.

ik~

0

0

~

Hl.2

a.

b.

Tem orar

S ent Fuel

Pool Covers

Ins ection Sco e

62707 92902

On May 28 and 29,

one of. the inspectors

reviewed the licensee's

maintenance activities associated

with Work Order

(WO) 97-004237-000,

. Remove Paint on

14WF I-Beams.

This involved removal of loose paint from

overhead

areas

on the refueling floor.

Covers were installed over the

spent fuel pools

(SFPs)

during the activities.

Violation 260/96-13-01

addressed

previous .maintenance

control deficiencies

associated

with

installation of the

SFP covers.

The inspector

reviewed the work

package,

held discussions

with involved workers

and supervisors,

and

inspected

the installed

SFP covers.

Observations

and Findin s

WO 97-004237-000 instructed workers to remove loose paint from the areas

in accordance

with Modification and Addition Instruction MAI-5.7

Painting

and Coating.

The

WO also referenced

Procedure

MSI-0-000-

PR0007, Installation and Re~oval of SFP Covers

and O-TI-264, Scaffolds

and Temporary Platforms.

The work package

contained the latest revision

of both procedures.

The inspector noted that the status of the ongoing

work was accurately indicated by the completed steps

signed off in the

WO.

By discussion with involved workers, the inspector determined that

no lead based paint had been

removed from the beams

so the precautions

required for such paint removal

were not applicable.

The inspector

reviewed the 50.59 safety assessment.

The assessment

was

performed in accordance

with Site Standard Practice

SSP-12.13,

10 CFR 50.59 Evaluations of Changes,

Tests,

and Experiments.

The assessment

focused

on the potential effects of the cover on the ability of the

SFP

cooling system to remove decay heat.

The assessment

stated that the

cover was to be installed after the evaporative/convectional

heat losses

from the pool would be insignificant compared to the

SFP cooling heat

exchanger

cooling.

The cover installation procedure

and the work order

contained

steps to require that at least

60 days

had passed

since the

last core offload and the pool was less than

125 degrees

F before the

cover was to be installed.

The inspector noted that the assessment

did

not address

potential effects of the cover on ventilation systems.

Subsequently,

the inspector

was informed by engineering that the cover

material

allowed air to pass through.

The inspector

concluded that

potential effects of the cover s regarding ventilation had been

satisfactorily addressed.

The assessment

adequately

addressed

other

issues

such

as combustible material loading.

The inspector verified that the covers were installed in accordance

with

the work control documents.

The cover

was fastened

as described

and the

ropes utilized were of the material

referenced in the safety assessment.

There was not a significant accumulation of material

on the covers

and

no holes were visible.

During the review, the inspector identified

several

problems associated

with foreign material exclusion practices

on

10

the refueling floor. Those deficiencies

are addressed

in Section Hl.3 of

this report.

c.

Conclusions

The inspector

concluded that the licensee

had developed

and was

- implementing .good maintenance

controls over the process of removing the

paint and installing the

SFP covers.

H1.3

Forei

n Haterial Exclusion

FHE

Practices

a.

Ins ection Sco

e

62707

During routine tours of the facility and observations of maintenance

activities, the inspectors

reviewed Foreign Haterial Exclusion

(FHE)

practices

and associated

documentation.

The inspectors

reviewed the

activities for compliance with Site Standard Practice SSP-12.8,

Foreign

Haterial Exclusion.

b.

Observations

and Findin s

During observation of several

maintenance activities and review of FHE

documentation,

the inspectors identified the following deficiencies:

The

FHE logs for the spent fuel pool areas

were not being

maintained in accordance

with the guidance in SSP-12.8.

FHE

monitors were not numbering the inventory pages properly, not

recording work activities and/or workers,

and not properly

updating the log after activities were completed.

It was

difficult to determine exactly what material

was inside the pool

areas,

particularly on Unit 2.

Step

12 of Section 3;5.A of SSP-12.8

requires that

a baseline

inventory be performed

and the log book reconciled prior to

activation of an

FHE area after it has

been inactive for greater

than seven

days.

In a majority of the cases

examined,

these

actions were not being performed

on the spent fuel pool areas.

Instruction 1.0.C of Appendix

E of SSP-12.8 states that clear

material

or other material

which would be difficult to identify

underwater shall not be used

on the Refuel Floor, unless

specifically authorized

by the refueling floor SRO,

SOS, or

Haintenance

Supervisor.

On Hay 29,

1997, the inspector observed

personnel

handling

a roll of clear plastic wrap material

on the

refueling floor.

The inspector determined that the material

was

being utilized on the refueling floor in support of health physics

activities such

as covering personnel

monitor detector

sensors.

On Hay 28,

1997, during review of WO 97-004237-000

documentation

(see Section H1.2), the inspector identified that Form SSP-62,

FHE

Requirements

Reference

Sheet,

was not filled out as required by

Section 3.2 of SSP-12.8.

Review of the

FHE logs indicated that

0

0

11

the proper levels of FHE controls were implemented in the 'SFP

areas

during the work.

~

On June 2,

1997, during review of WO 97-003911-000

documentation

(1B/1D residual

heat

removal

system heat exchanger cleaning),

the

inspector

identified that Form SSP-62,

FHE Requirements

Reference

Sheet,

was not filled .out properly.

The form indicated that

FHE

controls were required which'were not actually required

and were

not being implemented.

~

During observation of 1B residual

heat

removal

(RHR) heat

exchanger

cleaning,

the inspector

noted that no

FHE covers

had

been installed

on the

RHR service water lines which opened into

the heat exchanger.

Although SSP-12.8

does not contain specific

directions to install covers

on these

openings,

due to their size

and location, they appeared to be vulnerable to foreign material

introduction during the cleaning work.

The inspector discussed

these observations

with the involved workers and

plant management

upon identification.

The licensee's

FHE coordinator

reviewed the refueling floor FHE logs in detail

and initiated Problem

Evaluation Report BFPER970902.

The clear material

was removed from the

area

and BFPER970899

was initiated.

Haintenance

super vision corrected

the SSP-62

form, stopped the

RHR heat exchanger

work, and installed

an

FHE barrier on the

RHRSW piping openings.

Further, the licensee

reviewed

an additional

sampling of WOs and identified only one other

deficient Form-62.

The inspectors

had observed that overall

FHE controls during the recent

Unit 3 refueling outage were strong, with only one specific instance of

poor

FHE practices identified by the inspectors.

(See

IR 97-03)

In October

1994,

and in August 1995,

NRC inspectors identified

FHE

control deficiencies

which were violations of regulatory requirements

(IRs 94-27 and 95-51).

The inspector s reviewed the earlier violations

to determine if the most recent

issues

should be classified

as

a repeat

violation.

The earlier deficiencies

were mainly associated

with the

interior of the suppression

chamber.

Some aspects of the deficiencies

noted

above are similar to previously identified issues in that

implementation of FHE control processes

was not in accordance

with

procedures.

However, in the previous instances,

uncontrolled material

was actually found within, FHE control areas.

Violation 296/95-51-01,

Failure to Properly Control Haterial Within an

FHE Zone, involved torus area

FHE deficiencies.

The corrective actions

included significant programmatic actions to strengthen

the

FHE programs

at BFN. A single point of contact for

FHE issues

was established,

SSP-

12.8 was revised,

and

FHE monitor training was strengthened.

The

inspectors

concluded that the most recent deficiencies

wer e primarily

failures to follow administrative

processes

intended to ensure that

foreign material is properly controlled.

Unlike the previously

O~

0

0

C.

H1.4

a.

b.

12

identified FHE violations, this inspection did not identify any actual

cases of foreign material introduction into open systems.

Conclusions

The failures to follow procedure

SSP-12.8,

FHE Control, represent

a

.violation of 10 CFR 50, Appendix B; Criterion V.

The deficiencies will

be addressed

as Violation 260,296/97-07-02,

Foreign Haterial Exclusion

Controls not Implemented 'in Accordance with Procedures.

No actual

instances of foreign material introduction were involved, but

implementation of effective

FHE controls is important to safe plant

operation.

Although overall

FHE controls have been strengthened

since

1995, the recently identified deficiencies indicate that the

implementation of FHE administrative controls is not consistent.

Licensee Administration of the Inservice Testin

IST

Pro

ram

Ins ection Sco

e

73756 37551

The inspectors

performed

a review of the administration of the IST

program.

In accordance

with guidance

contained in IP73756

and IP37551,

the inspectors

reviewed the general

IST program and test results

of'arious

Residual

Heat Removal

(RHR) and Core Spray

(CS) system

pumps

and

valves.

Observations

and Findin s

During the inspection period, the inspectors

reviewed various aspects of

the licensee's

on-going IST program.

Five randomly selected

pumps

(two

from Unit 2, two from Unit 3 and one from Unit 1) and six randomly

selected

valves (three from Unit 2 and three from Unit 3) were chosen.

Test results

over the past

18 months of operation for the selected

equipment

was evaluated.

The following was indicated in this review:

3A CS Pump Performance

Was tested at least quarterly

Vibr Lvls 0.65 (+/- 0.15) mils

Total

Hd 233.80 (+/- 5.0) psig

2C

RHR Pump Performance

Was tested at least quarterly

Vibr Lvls 0.59 (+/- 0.30) mils

Total

Hd 267.50 (+/- 3.5) psig

1D RHR Pump Performance

Was test at least quarterly

Vibr Lvls 0.42 (+/- 0.20) mils

Total'd 266.20 (+/- 3.0) psig

3B RHR Pump Performance

Was tested at least quarterly

Vibr Lvls 0.65 (+/- 0.20) mils

Total

Hd 257.50 (+/- 2.5) psig

2D CS Pump Performance

Was tested at least quarterly

Vibr Lvls 0.38 (+/- 0.10) mils

Total

Hd 245.50 (+/- 4.5) psig

0

0

0

13

Loop I 'CS Iso Vlv 2-FCV-75-25

Was tested at least quarterly

Hax Closing Time Allowed - 30 sec

Average Closing Time

- 28.6 sec

Hax Opening, Time Allowed.- 30 sec

Average Opening Time

- 28.4 sec

P

3B RHR Pmp Inlet Vlv 3-FCV-74-24

Was tested at least quarter ly

Hax Closing Time Allowed

- 180 sec

Average Closing Time

- 117.8 sec

Hax Opening Time Allowed - 180 sec

Average Opening Time

- 121.1 sec

Loop I CS Iso Vlv 3-FCV-75-25

Was tested at least quarterly

Hax Closing Time Allowed - 30 sec

Average Closing Time

- 28.2 sec

Hax Opening Time Allowed - 30 sec

Average Opening Time 29.2 sec

Loop II CS Iso Vlv 2-FCV-75-53

Was tested at least quarterly

Hax Closing Time Allowed

- 30 sec

Average Closing Time

- '27.6 sec

Hax Opening Time Allowed - 30 sec

Average Opening Time

- '29'.1 sec

L'PCI Outbd Iso Vlv 3-FCV-74.-53

Was tested at least quarterly

Hax Closing Time Allowed

- 40 sec

Average Closing Time

- 33.0 sec

Hax Opening Time Allowed - 40 sec

Average Opening Time

- 32.4 sec

LPCI Outbd Iso Vlv 2-FCV-74-53

Was tested at least quarterly

Hax Closing Time Allowed - 40 sec

Average Closing Time

- 33.7. sec

Hax Opening Time Allowed - 40 sec

Average Opening Time

- 31.4 sec

C.

Overall testing methodology used for the reviewed

pumps

and valves

was

considered to be acceptable

and in accordance

with 10 CFR 50.55a

requirements.

Conclusions

The licensee's

current implementation of the IST progr am requirements is

adequate.

The licensee is conducting appropriate monitoring of safety

system valve and

pump operability.

Maintenance/Material

Condition of Facilities/Equipment

(61726,

62707)

.H2.1

Fire Protection

FP

Pi in

Re air /Re lacement

a.

Ins ection Sco 'e

62707

b.

The inspectors

observed corrective maintenance

repair activities

involving 12-inch

FP piping, replacement

on Unit 3.

Some repairs to 2-

inch

FP hose station piping were also obser ved.

In accordance

with

IP62707, the inspectors

performed field reviews of related piping

replacement

work orders

(WO 96-002856-000

and

WO 97-004887-000).

The

inspectors

also reviewed the overall status of FP piping given that

microbiological-induced

cor rosion (HIC) has

caused

some piping leaks.

Observations

and Findin s

On April 29,

1997, inspectors

obser ved repair activities being performed

on the Unit 3 12-inch

FP piping.

Repairs involved replacement of about

15-feet of 12-inch ASHE (ASA B31.1) standard

carbon steel piping.

The

repair was being performed because microbiologically induced corrosion

had caused

some pin-hole leaks in the piping.

According to the

WO,

il~

14

weldment information and work package,

nominal piping thickness

was

equal to 0.375 inches with a minimum calculated thickness of

0.328 inches

all.owable for the weldment.

The inspectors

noted that

during the original

"new piping to existing piping fit up," the existing

piping edge

was less than the allowable minimum.

A build-up of the

existing piping edge to greater

than 0.328 inches

was completed.

The inspectors

questioned

the licensee

about the actual wall thickness

of the remaining portions of existing fire protection piping.

The

licensee stated that ultrasonic testing of selected

areas of FP piping

had been performed

and that this testing indicated

some thinning of the

pipe walls (lowest points measured

were 0. 197 to 0.220 inches).

The

general

overall average

pipe thickness

was greater than the minimum

allowable, with 0.330 inches

average wall thickness.

The inspectors

also questioned

the licensee

about observed levels of

erosion

and corrosion in the old piping.

The licensee

acknowledged that

while some sediment

and general

corrosion

was found in much of the

FP

piping, the primary concern

was formation of microbiologically induced

corrosion sites (sites that were noted in low flow areas of the

FP

piping).

On Hay 21,

1997, the inspectors

observed the condition of the 2-inch

FP

piping removed from a hose station located in the facility's river water

intake structure.

Repairs

were being performed to replace patching that

had been

used for temporary repair of pin-hole leaks in the piping; 'The

interior of the piping contained

evidence of HIC and general

corrosion.

At one of the HIC sites,

a small through wall leak had occurred.

Given this information, the inspectors

questioned

the licensee

regar ding

confidence that

FP piping would not fail resulting in damage to

important plant equipment.

Additionally, the inspectors

discussed

whether loose corrosion products

or sediment

could potentially block

spray nozzles.

The licensee

has initiated actions to prevent

FP suppression

system

inoperability due to piping failures.

These actions

address

the

problems typically experienced

in raw water suppression

systems.

Several

engineers

described the licensee's

High Pressure

Fire Protection

Pipe- Replacement

Program.

The program addresses

replacement of the

major

above ground high pressure

piping headers

(wet) in the reactor

building, turbine building,

and diesel

generator buildings.

In the last

ten years,

more than one half of the originally installed

FP piping has

been replaced.

The program sets forth priorities for piping replacement.

Piping replacement

recommendations

are scheduled for several

years in

the future.

Host of the applicable piping in the Unit 2 and Unit 3

reactor buildings has

been replaced.

Unit 1 reactor

building piping

replacement is in progress.,

Significant portions of piping in the

turbine building has not been replaced.

il~

15

The inspectors

have noted that when leaks are identified in the

FP

piping, corrective actions are initiated.

The actions include

containment of leakage

and pipe patching

as necessary.

The licensee

stated that experience to date indicates that leaks in above ground

piping have been identified while still small in size (pinholes).

No

catastrophic failures of above ground piping have occurred.

Fire protection personnel

stated that the chemical treatment of the raw

water system which supplies the

FP system

has resulted in improvement in

the system conditions observed

dur ing testing.

For example,

during

flushing of strainers, little or

no material is found within the system.

Previously,

during some testing in previous years,

blockage of some

spray nozzles

had been noted but no longer occurs.

Conclusions

The inspectors

concluded that the on-going

FP piping replacement

and

repair program is adequate.

Overall, the licensee

has initiated

significant actions,

including chemical treatment,

which have improved

the reliability of the

FP suppression

systems.

The inspectors

concluded

that the licensee

has

an adequate

basis to conclude that

a sudden large

leak or rupture of'bove ground piping is not likely.

Haintenance

Procedures

and Documentation

Controls of Voluntar

Entr

Into Technical

S ecification Limitin

Conditions for 0 erations for Hodification Activities

a.

. Ins ection Sco

e

62707 92902

One of the inspectors

reviewed the licensee's

plan to remove

a train of

the Control

Room Emergency Ventilation .(CREV) System from service to

perform maintenance activities.

The inspector

reviewed the scheduled

work activities and the requirements

in Site Standard Practice

SSP-7.1,

Work Control; SSP-6.2,

Haintenance

Hanagement

System;

and SSP-9.3,

Plant

Hodifications and Design Change Control

0

b.

Observations

and Findin s

Early on June 5, 1997, the inspector

reviewed the approved detailed

planned work schedule,

which the licensee

commonly refers to as

a

"fragnet," for CREV 8 train charcoal tray changeout

per O-SI-4.7.E.4.B.

A fragnet is

a detailed schedule

which contains

a timeline of all

scheduled

work activities associated

with a particular system or train

of a system.

Work progress

and status is tracked against the fragnet by

the onshift and work scheduling personnel.

The inspector

noted that

approximately eight hours of the total scheduled

time for the planned

CREV train inoperability was associated

with Stage

4 of Hodification

T39971A (Work Plan 96-012074-002).

This work activity involved changing

the wire type/size

from the moisture element to the moisture transmitter

in flow loop 0-F-31-7213

(CREV B).

The inspector noted that, contrary

to most licensee

fragnets,

the time allotted fot the modification work

0

16

was not scheduled

in parallel with required corrective/preventive

maintenance

or testing.

Section 3.2.3 of SSP-7.1,

Voluntary Entry .into a Technical Specification

(TS) Limiting Condition for Operation

(LCO) for Modifications that

Result in Placing Unit 2 or Unit 3 in an

LCO, contains specific

. requirements for review and concurrence of'uch work during the planning

process.

These include Plant Operations

Review Committee

and Plant

Manager approval.

The work was scheduled to begin on the evening of

June 5.

The inspector questioned

the onshift Shift Technical Advisor

(STA) regarding

how these

requirements

were going to be met in this

case.

Subsequently,

the licensee

removed the modification work from the

fragnet

and performed only the preventive maintenance activity and

necessary testing.

This resulted in the train of CREV being inoperable

for a shorter duration.

The licensee's

work scheduling

group usually

controls the scheduling of such modification activities such that the

work is performed in parallel with required or necessary

maintenance

activities.

A TS

LCO is not typically entered in order to perform

modification work, but such work may be done if the system is rendered

inoperable for some other

work.

As such, the requirements of

Section 3.2.3 of SSP-7. 1 would not require specific review/approval.

The

inspectors

have not identified any similar previous examples.

No violation of regulatory requirements

occurred since the licensee did

not remove the system from service for the modification work.

The

inspector also noted that the SSP-7.1

requirements

do not distinguish

modification work which is corrective in nature.

Corrective maintenance

activities could be performed

as modification work.

Additionally,

Section 3.2.3 of SSP-7.1 refers to form SSP-226 which is entitled

Voluntary Entry Into a TS

LCO for Modifications on a Shutdown Unit That

Result in Placing an Operating Unit in an

LCO.

Apparently,

some of the

review requirements

were developed to ensure that restart

work

activities did not adversely affect an operating unit. At the close of

the inspection report period, the licensee

informed the inspectors that

a new Standard Practice is under development

which will include specific

procedural

guidance for controlling entry into TS LCOs.

Conclusions

The inspectors

concluded that this was

an isolated

case in which the

review for planned voluntary entry into a TS

LCO was not thorough.

Licensee

management

expectations for planning regarding entry into LCOs

for modification work were not met.

The equipment

was not .actually

removed from service

and corrective actions

were initiated immediately

when the inspector

questioned

the planned schedule.

NRC inspection of

Brown Ferry's implementation of the Maintenance

Rule was recently

completed (Inspection Report 259,260,296/97-04)

which included detailed

review of the licensee's

controls over removal of plant equipment

from

service.

No significant deficiencies

were identified. The licensee

il

ik~

M8.1

M8.2

H8.3

17

intends to revise procedural

guidance

regarding control of voluntary

entry into TS LCOs.

Hiscellaneous

Haintenance

Issues

(62707,

92902)

Closed

Violation 260/96-13-01,

Failure to Implement. Licensee-Approved

'ork Controls for Changes to the SFP.

This violation was caused

by a

failure to initiate work control processes

over the installation of

temporary covers over the spent fuel pools.

Section H1.2 describes

a

recent

NRC review of the implementation of work controls over the

covers.

The inspector

concluded that once the maintenance

controls

processes

were initiated, the licensee

implemented

good controls over

the activities.

The inspectors

noted that TVA has taken steps to

increase attention toward maintenance

controls over such activities.

The

violation is closed.

Closed

Licensee

Event

Re oct

LER 260/94-008-01

Containment

Penetration

and Hain Steam Isolation Valve Leak Rates

Exceeded

Technical

Specification Limits.

Revision

1 to this

LER provided additional

details regarding the causes

and corrective actions f'r the leak rate

test failures and repetitive problems.

The issues

involved with the

containment

purge valves were addressed

in Inspection Report (IR) 94-32

and Non-cited violation 94-32-01

was issued.

The original

LER was

reviewed

and closed out in IR 96-04'he inspector reviewed revision

1

of the

LER and concluded that no additional

NRC inspection is necessary.

Revision

1 of the

LER is closed.

Closed

Licensee

Event

Re ort

LER 296/95-005-00

A Residual

Heat

Removal Injection Valve was Inadvertently Closed

as

a Result of

Personnel

Error During Performance of a Troubleshooting

Work Order.

This incident involved a loss of shutdown cooling on Unit 3 prior to

fuel being loaded into the reactor

.

The major deficiency was that

troubleshooting

had not been properly controlled.

The issue

was

reviewed in detail by NRC inspectors

as described in Inspection Report

95-60.

Non-cited violation 95-60-02,

Loss of'hutdown Cooling Flow,

addressed

this issue.

The licensee

has continued to strengthen

troubleshooting controls, with recent

emphasis

given to pre-evolutionary

briefings.

This

LER is closed.

E1'onduct of Engineering

III. En ineerin

El.1

Outa

e Risk and

Hang ement

ORAH

S ent Fuel

Pool

Tem erature

Calculations

a.

Ins ection Sco

e

37551

During the most recent refueling outage,

the resident inspectors

noted

that the licensee's

Outage Risk and Hanagement

(ORAH) program

predictions for the temperature

increase of the fuel pool

and cavity

18

when shutdown cooling

(SDC) was secured

were not accurate.

The

prediction underestimated

the initial heatup rate

and actual

fuel pool

temperatures

increased

faster than predicted.

The inspectors

reviewed

the licensee's

actions to correct the problem.

The inspectors

also

compared the licensee's

refueling outage practices with the applicable

UFSAR descriptions.

b.

Observations

and Findin s

Following Spent

Fuel Pool/Cavity gate installation,

Spent

Fuel

Pool

temperature

increased

at approximately 2 degrees

F per hour, which was

higher than calculated.

The inspector questioned

the licensee

regarding the cause of the

differences

between actual

observed

temperatures

and the predicted or

calculated temperatures.

In response to the inspector 's questioning,

the licensee

determined that this was due to use of improper

differential temperatures

(the calculations

assumed

the pool

was at

a

constant

125 degrees

F).

This caused the calculated

heat

removal rate

to be higher than actual.

The licensee indicated that the model would

be improved.

The inspector

reviewed the licensee's

"outage lessons

learned" to

determine if the calculation problem had been addressed.

Although the

inspector did not find a specific lesson

learned

on the issue,

several

licensee

personnel

stated that the subject

was discussed

at the end of

outage critique.

The inspectors

also asked if any correlation could be made between the

observed

actual

performance of the

SFP cooling heat exchangers

and the

"design capability" referenced

in the

UFSAR.

The river was very cool

so

RBCCW temperatures

were well below the

"maximum" temperature

referenced

in UFSAR.

The licensee

responded

by stating that the

UFSAR

"capability" is that the

SFPCS

can keep pool temperatures

below 125

degrees

F when removing the maximum normal heat load from,the pool with

the maximum

RBCCW.

Section 10.5.5 of UFSAR,states this. (It should be

noted that supplemental

fuel pool cooling is available to use if

needed.)

The licensee

concluded that the observed

pool temperatures

did

not indicate any, problems with the SFPCS.

During the discussion,

the licensee's

reactor

engineers

discussed

that

calculations

are performed to predict when the pool gates

can be

installed after the fuel is offloaded.

The engineers

indicated that it

was well known that in some cases,

immediately following offload of'/3

of the core to the pool, the gates

could not be installed since

SFPCS

capability would not be high enough to remove the decay heat.

They

indicated that this is one of the primary reasons

for the pool heatup

calculations.

The licensee

does not consider this to be

a "difference"

with the way the

UFSAR describes

SFPCS heat

removal capacity.

The

licensee stated that this is part of the definition of "maximum normal

heat load." It was not clear to the inspectors that the licensee's

practices

are adequately reflected in the

UFSAR description.

The

UFSAR

E2

C.

19

does not imply or state that

some time for decay heat levels to decrease

may be necessary

before the

SFPCS

can maintain the pool temperatures.

Subsequently,

the licensee

provided documentation

which indicated that

as long as

15 days after .shutdown would be required before the

SFPCS

could remove the decay heat with RBCCW at 90 degrees

F..

The inspectors

have previously reviewed the licensee's

application of

the

ORAN programs.

The licensee

has consistently str ict)y controlled

installation and removal of the fuel pool gates.

Conclusions

The licensee

has initiated actions to address

the inaccurate

SFP

,temperature

calculations.

Although no actual

adverse effects

on

important plant equipment

have

been noted, additional

review of the

licensee's

practices

and the

UFSAR description involving SFPCS capacity

is warranted.

It was not clear to the inspectors that the actual

practices

are adequately reflected in the

UFSAR description.

Inspection

Followup Item 260,296/97-07-03,

Spent

Fuel

Pool Cooling

System

Heat Removal Capability,

addresses

this issue.

Engineering Support of Facilities and Equipment

E2.1

b.

Failure of the "28" Fuel

Pool Coolin

Pum

Ins ection Sco

e

37551

The inspectors

reviewed the licensee's

actions in response to a problem

involving the 28 fuel pool cooling (FPC)

pump.

Observations

and Findin s

On June 6, 1997, during a routine control

room tour,

one of the

inspectors

observed operator actions in response

to

a spent fuel pool

cooling system problem.

A fuel pool system

abnormal

annunciator

actuated

and the radwaste

operator

reported that there

was

a problem

with flow through the

FPC demineralizer.

An AUO investigated the

problem and reported that

FPC

pump discharge

pressure

(28

FPC

pump was

operating)

indicated about

20 psig and local flow indication was zero.

The 28

FPC

pump was running with a very high noise level.

The inspector

could hear

the

pump noise over the phone line.

The noise

sounded like

extreme

pump cavitation.

It appeared that the

pump was in runout

conditions.

The inspector

observed that the control

room operator s allowed the

pump

to run for several

minutes while they pursued the cause of the problem.

Their troubleshooting

focused

on the

FPC demineralizer valves

and

controllers.

Subsequently,

the 28 pump was turned off and the 2A pump

was utilized for cooling.

On disassembly,

the 28 pump impeller was.

found to be damaged badly.

An inner portion of the impeller had

0

20

separated

from the rest of the impeller.

At the close of the report

period, additional analysis of the failure was in progress.

The inspectors

reviewed the

FPC system drawings,

UFSAR descriptions,

and

operating procedures.

Discussions

were held with the system engineer

and engineering supervisory personnel.

The inspectors

were informed

that on Harch 26,

1997, the system engineer

had identified that the

pump

was operating in a runout condition.

Instrument mechanics

were

performing work on some level switches

associated. with the

FPC system

and it was believed that this played

a role in the

pump problems.

A lo-

lo fuel pool

skimmer

surge tank level condition had developed

during the

incident. After the incident, vibration monitoring of the 28 pump

indicated that bearing vibrations

had increased to the alert range but

not to a level at which operability would be affected.

Since the demineralizer portions of the Browns Ferry

FPC system are not

seismic,

the deminer alizer bypass

valves are designed to open on a

FPC

pump low discharge

pressure

signal.

This allows cooling flow to the

pool to be continued while the demineralizer portion is isolated

from

the pumps.

Engineering

had concluded that the full opening of the

bypass

valves

was causing the

pump to go into runout.

Engineering

had

initiated a work request

about

a month before the June

6 incident to

install stops to prevent the full opening of the demineralizer

bypass

valves.

The inspectors

noted that although the system engineer

and his

supervisor

pursued corrective actions to the problem,

a Problem

Evaluation Report

(PER)

was not initiated to address

the

Har ch 26

incident.

The inspectors

concluded that

a pump experiencing

runout

operation which was suspected

to be caused

by system operation

as it was

designed to operate,

should result in a

PER.

Plant management

was not

aware of the problem until after the subsequent

pump failure.

The inspectors

questioned

engineering

personnel

regarding their analysis

of the Harch 26, problem and the postulated

cause of. the

pump runout.

The inspectors

concluded that the cause of the lo-lo skimmer surge tank

level

had not been conclusively determined.

It also appeared that the

issue

had not been discussed

with other utilities or General Electric.

At the close of the report period, the 1-icensee

was continuing to review

the issues,

including the root cause of the

pump failure and actions to

address

the runout conditions.

PER 970946 addresses

the issues.

This

issue is identified as Unresolved

Item 260/97-07-04,

Fuel

Pool Cooling

Pump Failure. Additional

NRC review is necessary

when additional

information is available.

Conclusions

The control

room operators

actions following indications of pump failure

did not meet management

expectations.

Although engineering

personnel

pursued corrective actions to address

the postulated

cause of the

il

E8

21

Harch 26 incident,

a

PER was not initiated and plant management

was not

informed of the runout problem.

Additional

NRC review of this issue

will be conducted

when additional information is available.

Hiscellaneous

Engineering Issues

(92903)

E8.1

0 en

Ins ection Foll owu

Item

IFI

260/95-41-01

Emergency Diesel

Generator

(EDG) lA Turbocharger

Inspection.

On January

16,

1995, the

EDG was declared

inoperable

when it failed to go through the proper

shutdown

sequence

after

a stop signal

was initiated.

The

EDG was then

returned to operable status

on January

25.

1995.

Failure of the

turbocharger

planetary gear train initiated the event.

The planetary gears

supply the motive force for the turbocharger for

engine loads less than

70 percent.

At loads greater than

70 percent,

the exhaust

gases

provide the motive force for the turbocharger.

During

the event,

as the engine

was unloaded,

the available

amount of exhaust

gases

decreased'uch

that the turbocharger

should have been

dr iven by

its planetary gears.

Because

the gears

had failed, the turbocharger did

not supply sufficient combustion.air

and, therefore the

EDG shutdown.

The turbocharger

was immediately repaired

and returned to service.

The licensee's initial analysis identified "bending fatigue of a gear

tooth," on the turbocharger

sun gear,

as the most probable

cause of the

turbocharger

failure.

However,

a subsequent

analysis

determined that

the gear failed due to fatigue that was the resul,t of "quench cracking"

that occurred during manufacturing.

Earlier this year (IR 97-01) this

IFI was reviewed

and the inspectors

noted the results of a June

1996,

licensee-performed

metallurgical examination.

The inspectors

reviewed three laboratory reports

693.4A01,

693.A02,

and

693.A04 performed by Haterials Analytical Services,

Atlanta,

Ga. for EDG

Turbocharger

gear

crack examination,

sent

from TVA Browns Ferry Nuclear

Plant.

Report 693.A01 identified no cracks.

Reports

693.A02 and A04

identified that the gear failures were due to "quench cracking"

~

The

"quench cracking" allowed fatigue cr acks to propagate until catastrophic

failure of the gear

was presented.

The licensee

sent engineers

to visit

the vendor

(HKW Power Systems,

Inc.) for an inspection

and investigation

of the manufacturing process.

This visit and

a subsequent

licensee-

performed analysis confirmed preliminary conclusions that the "quench

cracks" were

a major contributor to the failures.

During the inspection period, the licensee

determined the root cause of

the failure to be manufacturing defects

and meetings

were held with the

turbocharger

manufacturer.

The manufacturer did not agree with the

licensee's

conclusion that the failures were caused

by manufacturing

defects

such

as quench cracking.

Pending additional review, IFI 260/95-41-01

remains

open.

However,

based

on the cur rent licensee analysis

and documentation,

associated

LERs96-001 (Revisions

0,

1 and 2) are closed.

f

II

E8.2

E8.3

E8.4

E8.5

22

Closed

Licensee

Event

Re orts

LERs

260/95-001-00

95-001-01

and 95-

001-02

OG Turbocharger

Failure That Resulted In Noncompliance With

Technical Specification Limiting Condition For Operation.

Section

E8. I

of this report describes

review of actions performed for IFI 260/95-41-

01,

Emergency Diesel Generator

(EDG)

1A Turbocharger

Inspection.

The

IFI addressed

the

same incident as the

LER.

Pending further review of

'he issue the IFI remains

open.

Based

on the review described in

Section E8.1, the original

LER and the two subsequent

revisions are

closed.

Closed

Unresolved

Item

URI

296/96-03-02,

Appendix

R Instrumentation

Discrepancies.

Inspection Report 96-04 contains

a discussion of a

detailed

NRC review of Appendix R issues.

In the report, the URI was

closed

for. Unit 2.

Violation 260/96-04-01,

Licensee Identified Appendix

R Deficiencies,

was opened to address

the issues.

The inspector

reviewed IR 96-04 and concluded that the concerns

associated

with Unit 3

were addressed

as well.

Due to an administrative oversight,

the URI was

not closed for Unit 3.

The URI is closed for Unit 3.

Closed

Licensee

Event

Re orts

LERs

260/95-008-00

and 95-008-01

Reactor

Zone Isolation Dampers Failed to Close.

The initial LER

addressed

a failure of two secondary

containment isolation dampers to

close

due to sticking solenoid valves.

Revision

1 of the

LER provided

additional details regarding the cause of these

damper failures and two

additional failures which occurred.

The sticking solenoids

were

attributed to a sticky residue

found at the core-plugnut interface in

the valves.

Revision

1 of the

LER states that further investigation is

in progress.

Replacement of solenoid valves with models which have not

exhibited the sticking problem has continued.

Inspection Report 95-64

describes

NRC review of these

issues

and related Information Notice 95-

53 'nspection

Followup Item 260,296/95-64-10,'econdary

Containment

Ventilation Damper Failures,

remains

open pending review of the

licensee's

longterm corrective actions.

The LERs are closed.

Closed

Licensee

Event

Re ort

LER 260/95-007-00,

Reactor

Scrammed

on

Loss of Main Condenser

Vacuum as

a Result of the Steam Jet Air Ejectors

Isolating on

a High Offgas Temperature.

The cause of the air ejector

isolation was traced to the failure of a power supply associated

with

the offgas condenser

water level control instrumentation.

The licensee

completed corrective actions to address

the failure.

The

LER is closed.

IV. Plant Su

rt

S2

S2.1

Status of Security Facilities and Equipment

Securit

Facilit

Observation

and Review

a.

Ins ection Sco

e

71750

On June 20,

1997, the inspector performed

a walkdown of portions of the

protected

area security fencing.

Additionally, the inspectors

toured

the Central

Alarm Station

(CAS) and the Secondary Alarm Station

(SAS)

~

i

23

during routine inspections.

Some of the activities were conducted

during deep backshift hours.

b.

Observations

and Findin s

The inspector discussed

several

observations

regarding the fence

'onditions with security personnel.

All items were adequately

addressed.

No significant problems were identified.

Inspectors

observed security personnel

in the

CAS and

SAS were alert and attentive

-to their duties.

V. Mana ement Meetin s

X1

Exit Meeting Summary

The resident inspectors

presented

inspection findings and results to

licensee

management

on June 24,

1997.

Other meetings to discuss report

,issues

were conducted during the report period.

A formal meeting with

plant management

was conducted

on June 3,

1997.

The licensee

acknowledged the findings presented.

Proprietary information is not

included in this inspection report.

PARTIAL LIST OF PERSONS

CONTACTED

t

Licensee

T. Abney., Licensing Manager

J. Brazell, Site Security Manager

R. Coleman, Acting Radiological Control

Hanager

J.

Corey, Radiological Controls

and Chemistry Manager

T. Cornelius,

Emergency Preparedness

and Planning

CD Crane, Site Vice President,

Browns Ferry

R. Greenman,

Training Manager

J.

Johnson,

Site Quality Assurance

Manager

R. Jones,

Assistant Plant Manager

S.

Kane, Acting Site Licensing Supervisor

G. Little, Acting Operations

Manager

K. Singer,

Plant Hanager

J. Schlessel,

Acting Maintenance

Manager

H. Williams, Site Engineering

Manager

INSPECTION PROCEDURES

USED

IP 37551:

Onsite Engineering

IP 40500:

Licensee Self-Assessments

IP 62707:

Maintenance

Observations

IP 61726:

Surveillance Observations

IP 71707:

Plant Operations

IP 71750:

Plant Support Activities

IP 73756:.

Inser vice Testing of Pumps

and Valves

t

IP 81502:.

Fitness

For Duty Program

IP 92901:

Foll owup-Pl ant Oper ations

IP 92902:

Followup-Ha'intenance

IP 92903:

Followup-Engineering

IP 93702:

Prompt Onsite Response

to Events at Operating

Power

Reactors

ITEHS OPENED

DISCUSSED

AND CLOSED

OPENED

~T

Item Number

'VIO

50-260,296/97-07-01

Status

Open

Descri tion and Reference

EOI Ladders

Not Adequately

Contr oiled (Section 01.1)

VIO

50-260,296/97-07-02

Open

IFI

50-260,296/97-07-03

Open

FHE Administrative Control

Procedures

Not Properly Implemented

(Section Hl ~ 3)

SFP Cool.ing System Heat Removal

Capability (Section E1.1)

URI

50-260/97-07-04

DISCUSSED

~T

Item Number

IFI

260/95-41-01

CLOSED

~T

Item Number

VIO

260/94-14-01-

VIO

260/96-13-01

LER 260/94-008-01

LER

296/95-005-00

n

Open

Status

Open

Status

Withdrawn

Closed

Closed

Closed

Failure Of Fuel

Pool Cooling Pump

(Section E2.1)

Descri tion and Reference

EDG lA Turbocharger

Inspection

(Section E8.1)

Descr i tion and Reference

Inadequate

Procedure Controlling

Voluntary Technical Specification

Limiting Condition For Oper ation

Entries (Section 08.1)

Failure To Implement Licensee-

Approved Work Controls For Changes

To The SFP (Section H8.1)

Containment

Penetr ation And Hain

Steam Isolation Valve Leak Rates

'xceeded

Technical Specification

Limits (Section H8.2)

A Residual

Heat Removal Injection

Valve Was Inadvertently Closed As A

Result Of Personnel

Error During

Performance

Of A Troubleshooting

Wor k Order (Section H8.3)

il

LER 260/95-001-00

LER

260/95-001-01

LER 260/95-001-02

URI

'296/96-03-02

LER 260/95-008-00

LER

260/95-008-01

LER 260/95-007-00

Closed

Closed

Closed

Closed

C,1osed

Closed

Closed

25

DG Turbocharger Failure That

Resulted

In Noncompliance With

Technical Specification Limiting

Condition For

Oper ation

(Section .E8.2)

Appendix

R Instrumentation

Discrepancies

(Section E8.3)

Reactor

Zone Isolation Dampers

Failed To Close (Section E8.4)

Reactor

Scrammed

On Loss Of Hain

Condenser

Vacuum As A Result Of The

Steam Jet Air Ejectors Isolating

On

A,High Offgas Temperature

(Section E8.5)

O~

ik

~

'