ML18033A944
| ML18033A944 | |
| Person / Time | |
|---|---|
| Site: | Browns Ferry |
| Issue date: | 08/29/1989 |
| From: | Carpenter D, Little W, Patterson C NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML18033A942 | List: |
| References | |
| 50-259-89-35, 50-260-89-35, 50-296-89-35, NUDOCS 8909130105 | |
| Download: ML18033A944 (47) | |
See also: IR 05000259/1989035
Text
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UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION II
101 MARIETTASTREET, N.W.
ATLANTA,GEORGIA 30323
Report Nos.:
50-259/89-35,
50-260/89-35,
and 50-296/89-35
Licensee:
Valley Authority
6N 38A Lookout Place
1101 Market Street
Chattanooga,
TN
37402-2801
Docket Nos.:
50-259,
50-260,
and 50-296
License Nos.:
and
Facility Name:
Browns Ferry Units 1, 2,
and
3
Inspection at Browns Ferry Site near Decatur,
Inspection
Conducted:
July 15 - August 16,
1989
Intpectort:
Q-.L
D.
R.
Carpe
er,
NRC
Ss te
M
hger
Q t4n,P
C.
A. Patt
'son,
NRC Rest t Coo
>nator
3'g
p~
Dat
S)
ned
Da e
S gned
Accompanied
by:
E. Christnot,
Resident
Inspector
M. Bearden,
Resident
Inspector
K. Ivey, Resident
Inspector
A. Johnson,
Project Engineer
Approved by:
.
S.
Li
e, Sect)on Chief,
Inspection
Programs,
TVA Projects Division
SUMMARY
D te
S gned
Scope:
This routine resident
inspection
included reportable
occurrences
and
action
on previous inspection findings.
Results:
Fourteen
LERS
were
reviewed
and
closed.
Fourteen
IFI's were
reviewed
and eleven
were closed.
Five violations were reviewed
and
one
remains
open.
Seven
URIs were closed with one being upgraded to
a
The
NOV involved operator
response
to
an off-normal condition,
paragraph
3. t.
The
two
NCVs concerned
design control to prevent
single failure and a missed SI, paragraph
3.u..and
s.
OO91.Q/Q5 89083i
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ADOCI< 0 0002
9
0
REPORT DETAILS
Persons
Contacted
Licensee
Employees:
~0. Zeringue, Site Director
- G. Campbell,
Plant Manager
"R. Smith, Project Engineer
J.
Hutton, Operations
Superintendent
A. Sorrell, Maintenance
Superintendent
D. Nims, Technical
Services
Supervisor
.
G. Turner, Site equality Assurance
Manager
P. -Carier, Site Licensing Manager
- P. Salas,
Acting Compliance Supervisor
J.
Corey, Site Radiological
Control Superintendent
R. Tuttle, Site Security Manager
Other
licensee
employees
or
contractors
contacted
included
licensed
reactor
operators,
auxiliary operators,
craftsmen,
technicians,
and
public safety officers;
and quality assurance,
design,.and
engineering
personnel.
NRC Attendees
- M. Little, Section Chief
"D. Carpenter,
Site Manager
"C. Patterson,
Restart
Coordinator
"E. Christnot,
Resident
Inspector
"M. Bearden,
Resident
Inspector
~K. Ivey, Resident
Inspector
A. Johnson,
Project Engineer
"Attended exit
interview'cronyms
used throughout this report are listed in the last paragraph.
Reportable
Occurrences
(92700)
The
LERs listed
below were
reviewed
to determine if the information
provided
met
NRC requirements.'he
determination
included
the
verification 'of
compliance
with
TS
and
regulatory
requirements,
and
addressed
the
adequacy
of the event description,
the corrective action
taken,
the
existence
of potential
generic
problems,
compliance
with
reporting
requirements,
and
the -relative
safety
significance
of each
event.
Additional in-plant reviews
and discussions
with plant personnel,
as appropriate,
were conducted.
a ~
(CLOSED)
LER
259,
260,
296/85-12,
Revision
1,
Design
Error in
Standby
Gas Treatment
Cable Routing.
A TVA modifications
engineer
found divisional cables
that
had been
routed
and installed
through
cable tray fire stop pressure
seals
using cables
designated
for nondivisional application.
In the
BFNP
0
I
Fire
Recovery
Plan,
cabling
was
added for use
as
spare
cabling.
This
cabling
was
intended
for
use
only in non-safety-related
circuits.
Due to
a
design
drawing error,
SBGT divisional cables
were routed
using
spare
cables.
A junction box was also determined
to
be seismically unqualified.
The cables
in question
could not be
,qualified
as
IEEE class
IE and
a design
change
was
processed
to
correct this.
The junction box
was acceptably
remounted.
The
NRC
inspector
reviewed the closure
package
for ECN P3208
and determined
the item had been satisfactorily resolved.
This item is closed.
(CLOSED)
Improper
Modification of
Secondary
Containment Relief Panels.
On
May 17,
1985,
during
a routine licensee
inspection,
the shift
engineer
observed
that explosive bolts
on the reactor
zone to the
refuel floor relief panels
had been replaced with standard -bolts and
nuts.
These
relief panels
serve
to prevent
excessive
pressure
differential
between
the reactor
zones
and the refuel floor during
design
basis
tornadoes
and
during
steamline
breaks
inside
the
reactor building.
The
NRC inspector
reviewed the
LER, dated
June
14, 1985,
and the
LER
closure
package
and
verified that it met
the
requirements
of
timeliness,
content,
and corrective
action.
The root
cause
was
determined
to
be lack of administrative
requirements
to ensure that
the
proper
explosive
bolts
were
used.
The licensee
replaced
the
substituted
bolts
with the
proper
designed
explosive
bolts
and
established
procedure
controls to ensure
adherence
to the special
requirements.
Procedure
MMI-14,
"Inspection
of
Secondary
Containment
Relief Panels,"
was
revised
to include all secondary
containment relief panels
in a scheduled
inspection
to ensure that
these relief panels
are
being properly maintained.
Based
on the
in-office and field review of the
LER and closure
package,
this item
is closed.
(CLOSED)
Drywell Control Air Isolation Valves Outside-
Design Basis
Because
of Design Modification Error.
This item is identical to IFI 260/87-33-02.
The IFI is being closed
and is discussed
in detail in Section
3 of this report.
This
LER is
closed.
(CLOSED)
Revision
1,
Unplanned
ESF Actuations
Due To
Inadequate
Procedures.
This item occurred
on August 3, 1988,
when Unit 2 received
spurious
low reactor
water
level
signals,
causing
several
ESF actuations.
The
spurious
signals
were
received
from
level
transmitters
2-LT-3-203A
and
2-LT-3-203B
when
clearances
were
released
on
transmitters
2-LT-3-206 and
2PPT-3-207 following modifications which
relocated
the
two instruments.
All four of these
transmitters
are
served
by
common
sensing
lines,
which were
drained,
cut,
and
rerouted
during the modification.
The workplan for the modification
did
not
include
back'iilling of
the
lines
following their
reinstallation.
The
SOS
was
aware of probable
ESF actuations
upon
removal
of the clearance
and therefore,
directed
IM assistance
in
returning
the
valves
to their
normal positions.
The
IM did not
understand
this to
be
a request
to actually return the instruments
to service
and did not backfill the lines prior to repositioning the
valves,
thereby initiating the low level signals.
The licensee
determined
the root cause to be procedural
inadequacies
which allowed
the
clearance
to
be lifted without
an
. adequately
coordinated
plan of action.
The following procedural
enhancements
have
been instituted:
Procedure
SDSP 8.4, "Modification Workplans,"
now requires that
workplans
be
reviewed
for potential
actuations
in
accordance
with
SDSP
7.9,
"Integrated
Schedule
and
Work
Contr o1. "
Procedure
SDSP
14.9,
"Equipment
Clearance
Procedure,"
now
requires
the
SOS to specify the proper
sequence
for equipment
restoration
when removing clearances.
The
above
procedural
enhancements
were reviewed by the
NRC inspector
and
appear
adequate
to preclude future events of this nature.
This
item is closed.
(CLOSED)
Unit 2 only, Battery Failure Concurrent With
LOP/LOCA Automatic Start of
RHR Pump.
On
March
3,
1988,
the licensee
discovered
during
a review of the
250V
DC system
a condition that involved a single failure of a logic
system
power
supply.
The fai lure of a battery supplying logic power
for division I of
RHR would prevent
one of the
two pumps in that
division from starting.
The other
pump in the division that
lost logic power receives
a start signal
from
RHR division II logic.
The battery failure also
causes
the start logic in division II to
sense
diesel
generator
power is available for the
RHR pump that lost
division logic when,'ue to the
LOP,
AC power would not be available
on
the
.,AC electrical
board
until the
diesel .generator
output
breaker
closes
after
the
time delay for the diesel
generator
to
obtain the rated voltage.
This energizes
the start relay for the
pump
and
causes
the breaker to try and close onto
a deenergized
electrical
AC board.
When this occurs,
the
pump breaker will trip.
The
pump
must
then
be
manual,ly
started
from the electrical
distribution board.
The licensee's
corrective action
was to initiate three
CARR's (one
for each
unit)
and to
implement
OCR 3549 through
ECN E-2-P7136.
This
ECN required
the installation of wiring and relanding of wiring
on specific
relays
and terminal points in the
shutdown
boards
as
indicated in Work Package
2182-88.
The
NRC
inspector
reviewed
the
documente'dc'or'rective
'actions,
observed
the
LOP/LOCA series
of tests
and considered
the action
appropriate.
This
LER i. closed for Unit 2 only.
The
NRC inspector
noted that this item is considered
part of the
BFN overall single
k
failure issue
and this
issue
is discussed
further in paragraph
3 of
thi s report.
(CLOSED)
Unplanned
ESF Actuation Caused
By Radiation
Monitor Power Supply Failure.
On
October
12,
1988,
while troubleshooting
using
a
maintenance
request,
instrument
mechanics
pulled the power supply for the Unit 2
reactor
zone
exhaust
radiation
monitor,
refuel
zone
exhaust
radiation
monitor,
and
offgas
system, carbon
bed vault radiation
monitor.
They observed
arcing
from a hole that
had been
burned in
the, high voltage
transformer
power
supply.
This arcing
caused
a
high radiation signal,
which resulted
in an
ESF actuation resulting
in a
SBGT train
B and
CREV train
B auto start.
The
NRC inspector
reviewed
the
LER and the
LER closure
package,
and
verified that it met the requirements
of timeliness,
content,
and
corrective
action.
The root cause
was
determined
to
be
a failed
power supply.
This
was
determined
by the General
Electric failure
analysis
which
stated
that
the failure
was
due to
component
degradation
through
aging,
aggravated
by the relative
lack of
reliability of
aluminum electrolytic
capacitors.
The
licensee
replaced
the
power
supply
and the
new power supply operation
was-
verified by performance
of the applicable surveillance instruction.
Based
on the in-office review of the
LER and closure
package,
this
item is closed.
(CLOSED)
Unplanned
ESF Actuations
Due
To Circuit
Protector Trip Caused
By Unstable
Relay Failure.
This
item involves
two identical
events
which occurred
10 minutes
apart
on
June
5,
1988.
The
lA1
RPS circuit protector tripped,
deenergizing
the Unit 1
Bus
1A and initiated several
engineered
safety features.
Following the
second
occurrence,
an investigation
was
initiated
which
determined
the
cause
to
be
an
unstable
relay in the circuit protector,
which tripped
when
subjected
to minor vibration.
The defective relay was replaced
and
returned
to the
manufacturer
for evaluation of potential
generic
problems.
,The manufacturer
determined
the probable
cause of failure
to
be
relay
contact
degradation
due
to airborne
contamination
creating corrosion
and pitting of the contacts.
The licensee
also
consulted
NPRDs to determine
whether similar failures of this type
relay
had
occurred
elsewhere
within the
industry.
No similar
failures
were
reported.
Therefore, it was
determined
that this
relay failure was
an isolated
case with no generic implications at
this time.
The inspector
reviewed the above actions
and evaluations
and determined
them to be appropriate.
This item is closed.
(CLOSED)
Revision 1, Operation
Over Spent
Fuel
Pools
Without
the
Minimum
Number
of
Standby
Gas
Treatment
Trains
This
event
involved
a
SBGT train
becoming
when
the
surveillance
period
required .by the
Technical
Specifications
had
expired.
The
SBGT train
was
subsequently
relied
upon to
meet
a limiting
condition for operation
action
statement.
This constituted
an
operation prohibited
by the technical specifications
and resulted in
the reportable
event.
Issues
related
to this event
are discussed
elsewhere
in this report
in
(paragraph
2.j),
and
260/88-35-02
(paragraph 3.s).
The
NRC
inspector
reviewed
the
event
description,
cause
and
corrective actions
and
found that the
LER met reporting standards.
This
LER is closed.
(Closed)
LERs
259/88-22
and
259/88-43,
Unplanned
ESF Actuations
Caused
By Radiation Monitor Upscale
Relay Failure
Both
LERs identify separate
unplanned
ESF actuations
resulting from
failures
of upscale
relay coils in the reactor
and refuel
zones
exhaust
radiation
monitoring circuity.
Both events
resulted
in
isolations
of the Unit 1 primary containment,
refuel
zone,
and
control
room ventilation
systems
and
initiated
and
systems.
The
NRC inspector
reviewed
LERs
259/88-22,
259/88-22
Revision
1,
259/88-43,
and
other
documentation
provided
by the licensee.
The
relay failures
were
due to undersized
relays in the original design.
In both cases,
corrective
maintenance
was initiated to replace
the
failed
relay.
Following repair,
the
radiation
monitor
was
functionally tested
and returned
to service.
The original
24 volt
Potter
Brumfield
KH4690 electromagnetic
relays
were
determined
by
the
licensee
to
be
undersized
when
continuously
operated
at
24
volts.
These
relays
are continuously energized
when in use
and fail
due
to deteriorati'on
resulting
from excessive
heat.
Industry
experience
has
shown that continuously
operated
relays
should
be
rated
at approximately
150K of their planned
operating
voltage.
This condition
had
been previously identified in
dated
July
30,
1976.
In the
above
LERs the licensee
states
that the
failure to implement the
recommendations
of the
matter
had
been
a contributing factor.
The failure to implement
this SIL was identified in July of 1987.
The licensee
had initiated
procurement
of new
36 volt relays but the
new relay's
had not arrived
at the time of the
two events.
Procurement
delays resulted in the
replacement
relays
not
being
available
for installation until
November 1988.
The
new
upgraded
relays
are
now installed in the
refuel
zone
and reactor
zone exhaust radiation monitors.
As part of
the corrective action to the
LERs the licensee
stated that vendor
information
is
now
reviewed
and
incorporated
as
required
in
accordance
with Volume I of the Nuclear
Performan'ce
Plan.
These
LERs are closed.
(CLOSED)
Unplanned
ESF Actuation.
This event
involves
two items,
the first was the discovery that the
"C"
SBGT Train was in operation
on December
13,
1988 for no apparent
reason.
The train was secured
and increased
security surveillance of
the
area
was provided.
There
was
on going work in the area.
The
second
item
was
the
discovery,
through
a surveillance
functional
test of the existence
of a undocumented inlet damper in the suction
ductwork of the
"C" train.
The "C" train was declared
the, damper
was
locked
open,
the system
was flow tested
and returned
to service.
A
CARR
BFP
881087
was initiated to investigate
and
correct appropriate
drawings
and procedures.
This
event is associated
with
Revision
1
(paragraph
2. h)
and
Unresolved
Item 260/88-35-02
(paragraph
3') and
are
discussed
further in this report.
A violation was issued in
NRC
IR 89-33.
The
NRC inspector
reviewed the event in association
with the above
related
issues
and the
CARR corrective action document.
The actions
proposed
were
adequate
and
were
implemented
in a timely manner.
This item is closed.
(CLOSED)
Design Error
On EECW,Discharge
Causes
Plant
To Be In An Unanalyzed Condition.
This
LER was associated
with the presence
of seismically unqualified
vitrified clay piping in certain
portions
of the
EECW discharge
flowpaths for various safety related
components.
Contrary to the
requirements
of
FSAR section
10. 10. 2. 2,
EECM piping was
found to
discharge
into non-qualified
24 inch
RCW discharge
These
24
inch
RCW headers
were routed
from the Reactor Building through the
RHRSW pipe tunnels
where they eventually
became
buried pipe and tied
into
30
inch
constructed
of vitrified clay.
During
a
seismic
event,
these vitrified clay headers
could collapse
and block
,the discharge
flow paths to the affected
components.
The licensee
reported
the condition to the
NRC on February 8,
1989.
The
circumstances
and
events
associated
with this
issue
are
discussed
in
greater
detail
in
NRC
Inspection
Report
259,
260, 296/89-10.
Any regulatory
concerns
associated
with this
issue will be followed as part of the open items identified in that
report.
This section will only address
the technical
resolution of
the non-seismically qualified discharge
piping.
Separate
plant modifications
are
intended to correct the problem by
rerouting
the- three
affected
EECM discharge
paths
to qualified
discharge
paths.
The licensee
has planned and/or performed work for
the following DCN's:
H5120A reroutes
piping associated
with both Unit 1/2 Control
Bay Chillers to qualified Unit 1
EECW 'discha'rge 'pipi'ng.
7
H5121A reroutes
piping associated
with Unit 2 Shutdown
Board
Room Coolers to qualified Unit 2
EECM discharge
path.
H5122A
reroutes
piping associated
with Unit
3 Control
Bay
Chiller 3A to qualified Unit 3
EECM discharge
path.
H5120A
and
H5122A were field complete
as of July 14,
and work on
H5121A
commenced
on July
18.
The
licensee
has
an
outstanding
commitment
(NC08900920021)
to complete all three modifications prior
to tensioning
the
Unit 2 reactor
vessel
head.
The
NRC inspector
considers
that
any concerns
associated
with the technical
resolution
of this issue
are satisfied.
This. item is closed.
(CLOSED)
Missed
Compensatory
Sampling
Mhile
Conductivity Nonitor Mas Out Of Service.
This
item
involves
the failure to perform
compensatory
reactor
coolant
water
conductivity
sampling
in Unit
3 at eight
hour
intervals
while
local
conductivity
monitor
3-CIT-43-011
was
as
required
by TS 4.6.B. l.c.
This compensatory
sampling
was
required
when
the local monitor was
removed
from service for-
repair and calibration.
Procedure
SDSP 7.9, "Integrated
Schedule
and
Mork Control," did not require
an IE to be performed
on this type of
instrument prior to allowing work to begin.
The
ASOS was not aware
that the monitor would be rendered
inoperable during troubleshooting
and recalibration,
thus,
the required eight hour sampling
was not
performed
for approximately
23 hours2.662037e-4 days <br />0.00639 hours <br />3.80291e-5 weeks <br />8.7515e-6 months <br />.
The licensee
determined
the
root cause
to
be the
inadequacy
in
SDSP 7.9 which did not require
the
performance of'he IE.
Had the IE been performed, all appropri-
ate
personnel
would
have
been
aware
of the
requirement
for
compensatory
sampling.
Procedure
SDSP
7.9
has
been
revised
to
require
specifically
to
be
performed
for
chemical
instrumentation
equipment
covered
by technical
specifications.
The
inspector
reviewed
the
above
actions
and
procedure
revision
and
determined
them to be appropriate.
Therefore, this item is closed.
(CLOSED)
Unplanned
Engineered
Safety
Features
Actuations
Caused
By Voltage Transient
On Electrical Distribution
System.
This
issue
is also
addressed
in IFI 260/88-28-03.
The IFI is
discussed
in detail
and
closed
in paragraph
3.m of this report.
This
LER is closed.
3.
Action o'n Previous
Inspection Findings (92701,
92702)
Q
a ~
(CLOSED)
IFI 260/86-40-03,
Unit 2 only,
IRN
Power
Supply
and
Procedure
Changes
Per SIL-445.
This
item
involves
procedural
enhancements
and
equipment
modifications
suggested
by General
Electric
During
an
outage
at
an operating
GE/BMR, all positive aiid negative
IRN 3/4
amp
fuses
connected
to the
24 vdc
bus
B were
blown because
of a power
e
surge
caused
by
a switching transient
on the
480V power
supply.
After the positive
3/4
amp fuses
were replaced,
all
IRM channels
were operating
normally.
However,
because
of continued loss of the
negative
power
supply
because
of the
blown fu'ses,
the
IRM channels
remained
and
unable to process
flux signals.
The=blown
negative
fuses
were
only detected
during
surveillance
testing
performed later
because
there
was
no blown fuse indication
on the
control
room
panels.
In view of the
above,
made
the
following recommendations:
Procedural
enhancements
to require functional testing of
and
IRM channels
to ensure
channel operability.
Replacement
of the
3/4
amp
IRM chassis
fuses
with 1.5
amp
fuses,
and
Modification to provide
a reactor protection
system
INOP trip
in response
to a loss of negative
24V power supply to the
IRMs.
As
a result of the
above
recommendations,
TVA has
performed
the
following actions:
Procedure
O-OI-57D,
"DC
Electrical
System
Operating
Instruction,"
Rev.
3,
Section
5.7. 12
requires
functional
testing of IRMs and
SRMs.
The
above
referenced,
fuse
replacement
and system modifications
have
been
completed,
for Unit 2 only, per
DCN-H1706A and Work
Plan 2583-88.
The inspector
reviewed
TVA's actions
and
determined
them to
be
adequate
to close this
item for Unit 2 only.
Units
1 and
3 will
remain
open pending completion of their respective
modifications,
b.
(CLOSED) IFI 259,
260, 296/86-40-12,
Potential for Overpressurization
of Residual
Heat
Removal
System. Piping.
This
item concerns
a modification installed to
reduce
excessive
pressure
drop
across
a throttling valve in the
RHR system.
This
item
was
reviewed
in
NRC Inspection
Report
259,
260,
296/88-32,
paragraph
9.e which concluded that the engineering
analysis
did not
consider
the design
basis
LOCA,
FSAR Section 14.6.3. 3. 2 where torus
pressure
co'uld
be
as high's
27 psig.
The basic issue is that the
portion of the
RHR system in question is rated at
150 psig, which
may
be
exceeded.
With the modification, which installed
an eight
inch orifice plate
downstream
of throttling valve
FCV-74-73, to
reduce
excessive
pressure
drop
across
that valve,
the
pressure
between
the orifice and the valve could be as high as
143 psig under
normal
conditions
with the torus at
atmospheric.
During
a
event,
the torus
could
be pressurized
to
27 psig which would mean
that the piping section could exceed
170 psig, in fact by worse case
calculation 173.8 psig.
0
e
The licensee's
reanalysis
confirms this data.
The
Code of record
for this
system
is
831. 1.0 - 1967.
Under Section
102.2.4,
Ratings:
Allowance for Variations
from
Normal
Operation,
the
following allowances
are provided:
(1)
Up to
15 percent
increase
above the S-value during ten percent
of the operating period.
(2)
Up to
20 percent
increase
above the S-value
dur ing one percent
of the operating'eriod.
For the
LOCA condition,
section
(2)
above
would apply, which would
allow
a
maximum pressure
of
180 psig during
one percent of the
operating
time.
Since
maximum analysis
pressure
would
be 173.8
psig,
the
system
would be within code allowable.
This consideration
is
consistent
with the
NRC's staff position
on similar
issues
resolved at SgN.
This item is closed.
(CLOSEO) IFI 259,
260,
296/87-FRP-01,
Closeout
TMI Item II.F.1.(3)
For Containment
High Range Radiation Monitors
(CHRRM).
The
item was
opened
in IR 87-33
as
a violation for an
inadequate
design modification package.
The
NRC inspectors
concerns
about the
modification
at
that
time
was 'that it
lacked
engineering
documentation
and calculations
to support evaluation of the adequacy
of the design.
TVA responded
to the item in a letter to the
NRC
dated
January ll, 1988
in which they maintained that design
and
justifications
met regulatory
requirements.
The
NRC concurred with
the
TVA position
and withdrew the
item in a letter to
TVA dated
October
31,
1988.
The October
31 letter also stated that the issue
would
be
identified
as
IFI 259,
260,
296/87-FRP-Ol,
because
of
several
deficiencies
described
with the violation.
The IFI was
opened
in
NRC inspection
report
88-14.
In that report the
NRC
inspector
discussed
the
system
design
and installation
as well
as
the fact that the
system
was not operable at that time and would be
subsequently
followed up in later inspections.
The
NRC inspectors
recent
review of this issue
revealed
that the
licensee
discussions
of system
design
in its violation response
provided reasonable
support in the that system design
met guidelines
,specified
in
met industry standards,
and is therefore
considered satisfactory.
The
licensee
provided
documentation
and
explanation
of concerns
raised
by the
NRC about the implementation of the modification that
were described
in IR 87-33.
These
documents
and discussions,
along
with
NRC inspectors
field observations
of the modification, indicate
that
the deficiencies
involving detector
orientation,
electrical
power
supply capabilities,
post modification retest
requirements,
and functional testing of the completed circuits have
been adequately
resolved.
Several
licensee
programs
exist that
are routinely
monitored
by the
NRC that will ensure the'eturn'to"service
of this
system.
These
programs
include:
LCO Tracking (this
system
is
10
required
by
TS 3. 2. F);
commitments
to complete
TMI items discussed
in
a letter from TVA to the
NRC dated
June
16,
1989; the licensee
return
to service
program,
and, System
Pre-operability
Checklist
(SPOC).
The
NRC inspector considers this item closed.
(OPEN) IFI 259,
260, 296/87-02-06,
Baseline
Walkdown Problems.
This item identified that the diesel
generator
starting air motors
were
not
shown
as part of the starting air system
in
FSAR figure
8.5-2.
The
licensee
prepared
a proposed'hange
to the
FSAR to
correct this
item.
The inspector
reviewed
the proposed
change
to
the
FSAR.
TVA has
requested
and been granted
a temporary
exemption
from
10 CFR Part 50.71(e) for an
annual
update
of the
FSAR.
The
change
wi 11
be
made
in the
July,
1990
update.
TVA is
maintaining
a "living" FSAR containing the proposed
changes
until
the
FSAR is
updated.
The inspector
reviewed
a controlled
copy
of the "living" FSAR in
Document Control
and
found the proposed
changes
in place.
Therefore, this item is considered
acceptable-for
restart
based
on the
temporary
exemption.
The item remains
open
since the original concern
has not been corrected in the
FSAR.
(CLOSED) IFI 259,
260, 296/87-20-02,
IE Notice Closeout
This
item concerns
the process
and
adequacy
of nuclear
experience
review activities.
Specifically, after
an action was identified as
being required at
BFNP based
on the nuclear
experience
review, the
item was
being closed
when the responsible
supervisor
stated that
a
particular action
was
committed to
be
done.
There
was
no followup
after
work was
committed
to
be
done.
The licensee
committed to
revise
the governing
procedures,
BFNP Standard
Practice
BF-21. 17,
Review,
Reporting,
and
Feedback
of Operating
Experience
Items,
and
to perform a gA audit of the experience
review process.
Since
NRC
IR 87-20,
the licensee
has
replaced
BF-21. 17 with
SDSP
15.9,
Nuclear
Experience
Review Program,
and performed the committed
gA audit.
The audit results
were
used in formulating
SDSP 15.9 and
in strengthening
the experience
review program.
There
were
22
Notices
identified in the
gA audit that
were
reopened
based
on
incomplete committments.
The
inspector
reviewed
SDSP
15.9,
Revision
5 and determined
that
it provides
adequate
guidelines
and
checks
to ensure
that nuclear
experience
review action
items
are
tracked until completion
and-
acceptance
of
the
required
action.
Section
6.3 of
SDSP
15.9
requires
the responsible
supervisor to retain Attachment
G, "Closure
of
NER Item," until the action
items
are fully implemented.
When
completed
and
returned
to
the
Site
Licensing
Manager,
Attachment
G tracking
on
the
and/or
TROI
data
base will
be closed.
The licensee's
action
on this item were responsive
and
acceptable.
This item is closed.
f.
(CLOSED)
IFI
260/87-33-02,
Fail ure
of
Drywel 1
Control
Air
Isolation Valves to Fail Closed
Upon Loss of Air.
During
performance
of Restart
Test
Procedure
-032,
the
drywell
control air suction
valves
(FCV-32-62
and -63) failed "as is" upon
loss of control air instead of failing closed,
as
was intended.
The
licensee
determined
the
cause of this malfunction to be the improper
implementation
of an
equipment modification intended to upgrade
the
solenoid
valves for environmental
qualification.
In addition,
the
following related
problems
were also noted:
Drawings
1-47E610-32-2
(Units
1
8 3) and 2-47E610-32-2 (Unit 2)
incorrectly depicted these
valves
as diaphragm valves.
Drawing 1-47E610-32-2
(Units
1
8 3) erroneously
indicated,
in
Note 8, that the air supply for these
valves in both units
was
drywell control air.
Th'ese
valves
were
found to
be missing
from
FSAR Table 7.3-1,
"Pipelines Penetrating
To correct
these
problems,
the licensee
has
completed
the following
actions:
The Unit
2 valves
have
been
replaced
per
ECN W0690
and work
plan 2353-88,
and were successfully
retested
on May 22,
1989 per
2-BFN-RTP-032,
CN-08.
Drawing
2-47E610-32-2
has
been
revised to identify accurately
the valves
as air operated-vane
drive motor plug valves.
Amendment
6 to
the
incorporated
these
valves
into
Table 7.3-1.
The
inspector
reviewed
the
above
completed
actions
and
determined
them to address
adequately
the identified problems
as
they pertain
to Unit 2.
Therefore,
this item is closed for Unit 2, but will
remain
open for Units j. and
3 pending
completion of the necessary
hardware
modifications
and drawing deficiencies.
In addition,
the
licensee
had also reported
the valve malfunction in
This
LER is closed in paragraph
2.c of this report.
g.
(CLOSED) IFI 260/87-37-03,
Reactor Mater Level Sensing
Lines.
This item involves questions
pertaining to licensee's
resolution of
the
February
13,
1985 reactor water level
mismatch
event.
General
Electric
had performed
a review of the event
and submitted
a report
to
TVA containing conclusions,
determination
of probable
cause,
and
recommendations.
This
report
was
an
attachment
to
GE letter
G-ER-6-333,
dated
August 21, 1986.
The cause of the above event
was
determined
to
be the rigid instrument piping system which would not
permit adequate
movement
upon thermal
growth of the reactor vessel.
To correct
the problem, the rigid instrument piping system in Unit 2
has
been
replaced
with a modified flexible system in accordance
with
E-2-P7131,
which completed all modifications to Reactor
Water
Level
Instrumentati on
necessary
to
suppor t
Unit
2
restart.
Therefore, this item is closed for Unit 2 only.
During the review of documentation
associated
with the installation
of the flexible instrument piping system,
additional
concerns
were
observed.
The
new installation is
comprised
of 1 inch diameter
stainless
steel
piping, with spring-can
hangers utilized to provide
. the desired 'flexibi.lity.
As Unit.,2 is currently in a cold shutdown
condition,'ost-modification
testing
could verify only the "cold"
settings
on
the
spring-cans.
The
"hot" settings
can
only
be
verified
when
the reactor
reaches
or nears
operating
temperature.
The
review of the
documentation
provided,
and conversations
with
licensee
personnel
indicate that,
due to the cold position of the
spring-cans
and the actual
length of the springs,
the expected
hot
position setting will be
adequate
when
the reactor
achieves its
expected
thermal
growth.
However, at present,
there are
no plans to
verify physically
these
hot settings
and engineering
calculations
have not been provided to support the above conclusion.
. A- second
concern
involves preventive
maintenance.
The previously
referenced
GE report contains
a statement
which reads
as follows:
"The drywell instrument line piping in all
3 units appeared
to have
been
designed
for flexibility, but was
a rigid system.
The rigid
system
appears
to
have
evolved
from the years
of operation
and
absence
of plant maintenance
of small
diameter piping."
When the
inspector
questioned
licensee
personnel
as to what actions
had been
or
would
be
taken
to
address
GE's
assessment,
no
evidence
was
provided
to
indicate
that
the
question
of maintenance
and/or
periodic inspections
had
been
considered
nor were
any
such actions
anticipated
in the future.
It should
be
noted that ISI programs
cannot
be
relied
upon
for these
lines,
as
ASME Section
XI
specifically
excludes
ISI requirements
for 1" diameter
and
under
piping
systems.
Resolution of these
concerns
involving preventive
maintenance
and verificaton of hot spring-can
hanger
settings will
be
tracked
as
inspector
followup item IFI 259,
260, 296/89-35-01.
This is not
a Unit 2 restart
item but programmatically it should
be
, addressed
during the
power ascention
testing,
prior to full power
operation.
(CLOSED) IFI 260/87-42-03,
ECN L2003 Closeout.
This
item concerned
work performed
under
L2003 which involved
licensee
action in response
Inspection of
BWR Stainless
Steel
Piping.
This
ECN was to replace
304 series
stainless
steel
piping in system
75,
Core Spray, with carbon steel
to reduce
the potential for intergranular stress
corrosion cracking.
The IFI noted that
several
3/4
inch drain
and test lines
were
omitted from the
ECN and would thus remain stainless
steel.
0
13
The
NRC inspector
reviewed Safety Evaluation
L2003, Revision
3 dated
October
28,
1988,
which addressed
concerns
for small
piping in the
system.
NRC Po'sition
on
IGSCC in
BWR Austenitic Stainless
Steel
Piping, states
that this
GL superseded
the requirements
of GL 84-11.
It further states that
the requirements
of GL 88-01
do not apply to piping less
than four
inches
nominal diameter
regardless
of code classification.
Based
on the revision of the
and
guidance
of GL 88-01,
the
licensee
does
not intend to replace
the 3/4 inch drain
and test
lines
of
system
75.
This is consistent
with the
NRC's staff
interpretation of the
IGSCC requirements.
This item is closed.
(OPEN) IFI 259,
260, 296/88-04-04,
Single Failure Criteria Involving
Emergency
Core
Cooling
Systems
Identified as
Part of the Restart
Test Program.
This
inspector
followup
item
involved
a
licensee
identified
condition
where single failure design criteria
was not applied to
the design
of* subsystem
280, Battery Boards,
and subsystem
231,
and
the 480 Volt AC SDBD.
The finding was documented
on
CARR BFP 880067,
Revision
1.
These
two issues
represent
significant
examples
of
design
program. deficiencies.
These
and
other
examples
of single
failure violations are
discussed
elsewhere
in the report along with
the corrective
actions
to improve the design control program.
This
IFI involves only equipment modifications associated
with
CARR
BFP
880067.
CARR
BFP 88067 discusses
two
DC power systems:
the
250V
DC battery
supply that the
TS refer to as station unit batteries,
and the
250Y
shutdown
board batteries.
The unit batteries
supply certain safety
related
loads
such
as
HPCI-valves
and containment isolation valves.
The
SD battery
board supply provides control
power for the load shed
logic of the 4160V AC shutdown boards.
The
CA(R stated
the loss of the
250V
DC Unit Battery Board
1 would
result in the loss of the
DC control
power for the load shed logic
features
to the 480V AC SDBDs
SDBD lA (Unit 1, Div 1)
SDBD 1B (Unit 1, Div 2)
and in the
loss of core
spray logic for Unit 1, Division 2.
This
violated single failure because
two divisions
were affected
by one
failure.
Loss of this load
shed
feature
during certain accident
conditions
will result
in overloading
the
associated
diesel
generator.
The
480V
AC shutdown
boards 'are
supplied
from the associated
4160V
SDBDs.
The resolution of this problem
was the
reassignment
of the
250V
control logic power supplies
of the 480V AC shutdown boards lA, 2A,
1B and
2B from the unit batteries
to the 4160V AC SDBDs,
250V DC SDBD
batteries
(SB-A, SB-B, SB-C,
and SB-D).
Now with the failure of a single
DC control
power source
such
as
SB-D, only the associated
4160V
AC board, its diesel
generator,
and
the
480V
boards
fed
from them
would
be affected,
thereby
preserving single failure design criteria.
TYA implemented
the resolution of this problem
by performing work
associated
with ECN's
E-2-P7117
and
E-2-P7124
which reassigned
the
source of normal
480V SDBD control power feeds.
The inspector
reviewed
the
documents
provided
by the
TVA licensing
section
for
closure
of this
issue.
The
implementing
work
instructions
appeared
satisfactory.
The
NRC inspector
observed that
the safety evaluation
associated
with this modification specified
no
TS
changes
would
be
necessary.
The
10 CFR 50.59 evaluation
did
state
that the
bases
for auxiliary electrical
equipment,
section 3.9
of the
TS would need to
be revised.
A review by the inspector of
the
complete
TS
revealed
that this plant modification
caused
a
confusing relationship
between
two different limiting conditions.
TS 3.9.8.4 entitled "Operation with Inoperable
Equipment", requires
initiation of
and orderly shutdown within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> if a 4160V
shutdown
board
and
any
480V
AC emergency
power
shutdown
board
are
at the
same
time.
This condition,
loss of a 4160
and
a
480V
AC board, will occur anytime
a
250V
DC shutdown board is made
This is
the result of the recent modification that
aligns
the
250V
DC shutdown
boards
to supply control power to both
of the associated
AC shutdown boards.
TS 3.9.B.8
addresses
the
loss of a
250V shutdown battery or its
associated
battery
board,
and permits
continued reactor
operation
for up to five days if a
250V shutdown battery or battery board is
Since
the loss of any
250V
DC shutdown
board
now always results in
the
loss of control
power,
to both
a 4160V AC and a 480V
AC board,
TS 3.9.B.4,
and
3.9.B.8 are conflicting with one another.
The
NRC inspector
considers
this IFI as
open until the conflict
between
TS 3.9.B.8
and
3.9.B.4V is
resolved.
This is
a Unit 2
restart
issue.
(OPEN)
IFI
259,
260,
296/88-05-06,
Potential
Single
Failure - Two Sets
of
Two
From
Two Trains
are
Actuated
Thru One Relay.
This
issue
represents
a
design
deficiency that pertains
to the
secondary
containment
isolation
system.
Four ventilation
located
in the
equipment
bay
(Drawing 47E865
Damper¹
1-FC0-64-65A,
B,
C and D),
between
the inner and outer equipment doors,
were found
to close
on
an initiation signal
from either of two trains of the
SBGT.
The
two signals
actuate
the
same
single relay which closes
- .. =
all
four
Failure of this relay
would prevent
proper
operation of all four dampers.
15
This
item
was identified
as
a result of the Restart
Test
Program
(RTP-65-SBGT)
and
documented
by
on
CAQR
BFT 880186.
The
resolution of the
CAQR was to rework the
system
design
and return
the
system
to
one that
meets
design
requirements
pertaining
to
single failure.
The
work will not
be
performed until the next
refueling cycle.
Therefore
the
system
hardware is to remain
and
certain
compensatory
actions
will
be
,implemented
to
provide
assurance
that
the
system
functions will be
met.
This action is
effectively
a use-as-is
disposition to
a non-conforming condition,
at least
for the interim period before
the
hardware
is reworked.
The
use-as-is
disposition
is
a
design
output;
a modification of
design criteria
and therefore
requires
a
10 CFR 50.59 review.
The
NRC inspector
could find no 50. 59 review associated
with the
CAQR.
TVA was notified of the inspectors
concern
on August 8, 1989.
This IFI wi 11
remain
open until a documented
10 CFR 50. 59 evaluation
is provided or performed.
Review of other
CAQR's despositioned
as
rework or use-as-is
should
be performed to ensure that
a trend of such oversights did not exist
in
previous
CAQR
resolutions.
The
current
CAQR
program
is
documented
in
SDSP
3. 13,
Revision 2, "Corrective Actions,"
and in
concert
with
NEP 6.6,
Revision
1,
Evaluations,"
provide
reasonable
assurance
that recently dispositioned
CAQR's are
not vulnerable to problems that existed in the earlier program.
k.
(CLOSED)
IFI
259,
260,
296/88-21-04,
Deficiencies
Identified
During Retest of LOP/LOCA C.
This item involves the failure of the
Pump
2A breaker to close
automatically during performance
of LOP/LOCA test
C in July 1988,
as
required
by procedure
2-BFN-RTP-L/L-C, Revision
2.
Upon discovery,
an unsuccessful
attempt
was
made to manually close the breaker
from
the control
room.
The following actions
were then taken:
Voltage
measurements
taken in the breaker
control
compartment
revealed
that the positive side of the
250V
DC close signal
was
present
up to the breaker position switch.
=
The
breaker
was
removed
from
its
compartment
for
troubleshooting.
All components
associated
with the charging,
closing,
and tripping circuits were
checked,
revealing nothing
that would indicate
a lack of continuity in the positive
250V
DC closing circuit.
Secondary
disconnect
pin
HG2 was observed to stick slightly and
showed
signs
of arcing.
The pin
was
cleaned
with contact
cleaner
and exercised
several
times to eliminate the sticking.
Inspection of the breaker
compartment
revealed
the guide rail
in the bottom center of the
compartment
to be bent.
The rail
was straightened
and proper alignment verified.
16
The
breaker
was
racked
back into its
compartment,
tested
several
times,
and observed
to -be functioning correctly.
Subsequent
licensee
evaluatio'n
of the
above actions
and findings
determined
the probable
cause
of the failure of the breaker to be
slight misalignment
(due to the bent guide rail) in conjunction with
the sticking
MG2 pin.
These actions
and evaluations
were documented
on
TE -05, Maintenance
Request
908524,
and CA(R-BFP880518.
As previously reported
in
NRC
IR 88-24, at the request of NRC, the
PM records for this breaker
were reviewed.
It was revealed that
had not been
performed
on this breaker
in three years.
The failure
to perform the
required
PM on this breaker
and
on safety-related
.
4. 16
KV breakers,
i'n general,
resulted in the issuance
of Violation
259,
260,
296/88-24.-08.
Therefore,
as this specific breaker
has
been
adequately
addressed,
and
as
programmatic
corrective
actions
regarding
on
4. 16
KV breakers
is
being tracked
by the
above
violation, this item is closed.
(CLOSED)
IFI
259,
260,
296/88-21-05,
Vaulting of Completed
and
Approved Test Results.
This concern
was originally identified by the inspector
during the
continuous
observation
of the
RTP.
The inspector
reviewed
SDSP 2.5,
equality
Assurance
Records,
and
noted that completed
gA records
may
be, stored
up to
30
days in fire resistant
metal file cabinets.
The
NRC inspector
observed
that
gA records
were being maintained in
fire resistant
metal file cabinets
with restricted
access.
This
item is closed.
During
the
above
review,
an
additional
concern
was
observed.
SDSP 2.5,
Revision
9,
page
nine
contains
a
note
specifying
requirements
for temporary
storage
of gA records..
There is one set
of requirements
for records
being temporarily stored for 60 days or
less,
and
a second set of requirements
for records
beings temporarily
stored
for more
than
60
days.
TVA Topical
Report
TVA-TR75-1A,
Revision
10,
Table
17D-2, Sheet
7 makes
no allowance for temporarily
storing
gA records for periods
in excess
of 60 days.
This concern
is identified
as IFI 259,
260,
296/89-35-02,
pending resolution of
this
potential
conflict
between
the
commitment
and its
implementing
procedure
and
should
be
addressed
prior to restart
of Unit 2.
(CLOSED) IFI 260/88-28-03,
Spurious
RPS Trips Associated
With
Alternate
Power Supply and Circuit Protectors.
NRC
IR 88-28 identified the concern that
many spurious
RPS trips
were being actuated
by the
RPS circuit protectors.
This issue
was
also discussed
in IR 89-11.
The
RPS for each of the three
BFN units is divided into two trip
systems
(A and
B) and both systems
are provided with a
MG set.
The
MG sets
are
powered
from the
480
V auxiliary power system.
Each
unit also
has
a
single
maintenance
power
supply (alternative
e
,17
transformer)
that
can
be aligned to either
RPS distribution system
A
or
B,
but not at the
same
time.
Circuit protectors. are provided
between
the
output
of the
MG sets
and
the
breakers
for. the
associated
RPS distribution
bus,
and
between
the
output of the
regulating
transformer
and
the
connection
switches
to the
distribution.
The circuit protectors will open to disconnect
the
RPS distribution
on
under
voltage,
over voltage, or under frequency
conditions.
After the Unit 3
loss of power event
on March 7,
1989 (see
IR
89-11,
paragraphs
4 and 8) the licensee's
system engineers
issued
a
report
on
RPS circuit protector
performance
and
made
recommendations
for minimizing or eliminating circuit protector problems.
The
NRC inspector
reviewed the licensee's
report
and discussed
the
status
of the
recommended
actions
with the
cognizant
system
engineer.
The
NRC inspector verified that the licensee
performed
the following actions:
o
Operating
and
PM instructions
were revised to minimize the time
that
RPS buses
are left on the alternate
supply transformer,
o
Testing
of the
MG set
voltage
regulator
was
performed
and
instructions
for their
inspection
and
cleaning were enhanced.
o
Modifications
to
improve circuit protector reliability were
initiated.
The cognizant
system
engineer
stated
that these
actions
were taken
to
provide
better
performance
of the current circuit protector
design
and
to minimize the
chances
for spurious
trips.
System
engineering
also
requested
that
ONE reevaluate
the basis for the
circuit protector relaying setpoints,
reevaluate
the current
use of
time
delays
in
the circuit protectors,
and
perform
a safety
evaluation
to determine if the Unit 1 and Unit 3 circuit protectors
could
be
bypassed
unti 1 unit refueling.
These
actions
were not
complete at the
end of this reporting period.
The system engineer
stated
that these
evaluations
could
be
used to enhance
the current
systems
performance
but are
not
necessary
for it to provide its
intended function.
The
NRC
inspector
concluded
that
the
licensee
had
adequately
addressed
the
concerns
raised
by this item,
had taken actions
to
preclude
recurrence
of spurious trips,
and
were actively pursuing
actions
to
enhance
the current design.
This item is closed.
In
addition,
the
licensee
reported
the Unit 3
RPS loss of power in
LERs 296/89-03
and 259/88-18.
These
LERs are closed in paragraph
2
of this report.
18
'CLOSED)
IFI 259,
260,
296/88-32-02,
Diesel
Generator
RTP Test.
This item was originally identified by the licensee
and involved a
review of the
system
82,
DGs,
RTP test
procedure
results.
This
review indicated that
the
section of the procedure
involving the
test
of the
3A
was either
not performed
or
was
inadequately
documented.
A decision
to perform the
test
on
3A
DG was
made
and section
5. 7,
Load Run,
Load Acceptance
Test,
and Miscellaneous
Tests,
Data Sheet
7.21 of RTP-082
was performed
on
October
27,
1988.
The
NRC inspector
reviewed
data
sheet
7.21 .and
noted that
the
test of the
3A
DG was successful.
This
item is closed.
(CLOSED)
259,
260,
296/87-02-05,
Ambiguous
Surveillance
Intervals.
This item involved
by plant technical
once
per operating
old.
This applied
at all times.
the fact that certain surveillance tests
required
specifications
to
be performed at a frequency of
cycle had performance
dates
as
much as four years
to some
systems that were required to be operable
This
condition
was identified
because
of the duration
of this
shutdown period for the Brown's Ferry Units started
May 1985 and the
wording of the plant's
custom
TS.
Standardized
TS generally specify
18
months
as
a refueling
and operating
cycle.
This permits
the
application
of period
extensions
as
well
as
a bounded
period of
time.
TVA evaluated its surveillance
testing
program in its response
to
this
URI with the stated
intent of identifying tests
scheduled
on
a
once
per operating
cycle frequency that would more prudently be on
an
18 month frequency..
The investigation,
completed
in June
1987
indicated
44 survei llances
should
have their frequency
upgraded.
The
tests
were
primarily
on
secondary
containment
systems
and
control
room 'emergency ventilation.
The review also determined that
the tests
identified for
upgrade
had been performed in the prior 18
months.
TVA also
revised
SDSP 12.7,
"Systems Pre-operability Checklists," to
require
review of once-per operating cycle surveillances
to evaluate
whether
the
needs
to
be reperformed prior to declaring
a system
The inspector
reviewed
the issue
and
TVA's corrective actions,
and
found that
the
program for scheduling
of the
once
per operating
cycle
surveillances
had
been
effective
as
evidenced
by
the
successful
reperformance
of previously
identified SI's
as
they
approached
an
18 month period since their last performance.
SDSP
12.7
was
reviewed with no
comment.
The
NRC inspector also reviewed
the
plant's
book
of
TS interpretations
for"the "purpose
of
determining if an official TVA position
had
been
documented
on the
19
once
per
operating
cycle
issue.
The
inspector
found
an
interpretation
discussion
on
TS wording of surveillance
frequencies
but the discussion
did not include the "once per cycle" issue.
This
point
was
brought
to
the
attention
of l.icensing
personnel.
Licensing
responded
with assurance
that
an 'expansion
of the
interpretations
would
be
considered
to
ensure
long
term
and
consistent
understanding
of the frequency issue until appropriate
TS
changes
were approved.
The
inspector
occurred
as
a
actions
taken
high level of
be
performance
of
closed.
determined
that
no violation of
NRC 'equirements
result of long surveillance
periods.
However,
the
by
TVA arq
expected.
to remain in place to ensure
a
confidence. will be maintained
in systems
required to
This
confidence will be obtained
by the successful
regularly scheduled
surveillance tests.
This item is
(CLOSED)
259,
260,
296/87-26-02,
Adequacy
of
Sampling
Program for Resolution of IEB 79-14,
Phase I Deficiencies.
This
item
involves
the
question
as
to whether
TVA's proposed
sampling
program
would
be
adequate
to resolve
concerns
regarding
pre-1985
walkdowns of piping supports
pertaining to IEB 79-14.
proposed
to perform walkdowns of 60 supports
to determine as-built
configurations,
'and
then perform evaluations
of these configurations
to determine
support
adequacy.
The results of this sampling program
were
intended
to provide
an acceptable
level of confidence
in the
Phase
I walkdowns
performed prior to 1985.
Subsequent
reviews
by
NRC staff have
determined
that the
proposed
sampling
program would
not
provide
adequate
assurance
as
to the
accuracy
of pre-1985
walkdowns.
Therefore,
TVA has
been directed to perform 100K of the
Unit
2
Phase II walkdowns
and
subsequent
engineering
evaluations
prior to restart.
These
directions
are contained in NRC letters to
TVA dated
March 25,
1988 and June
19,
1989.
Because it has
been
determined
that TVA's proposed
sampling program
cannot
be utilized in conjunction
with the overall
program,
and
as
future
NRC reviews
of the results
of the
100%
walkdown
and
evaluation will be performed
as part of the overall
assessment
of TVA's 79-14 program, this item is closed.
(Closed)
259,
260,
296/88-28-05,
Failure
to Report
Loss
of
Cooling Water to Diesel Generators.
During
an overheating
event
associated
with the
3C
DG that occurred
on September
29,
1988, the licensee
operated
the
DG for surveillance
testing with, no cooling water available.
The north
and south
had
been unintentionally isolated at
an earlier date
from
the four Unit 3
due to a valve alignment problem resulting from
a
known
drawing
discrepancy.
The
condition
which
would
have
resulted
in both divisions of safety-related
electrical
equipment
failing went undetected
for three
days.
'A contributing factor to
this
problem
was the
absence
of either local or remote
EECW flow
20
instrumentation.
Violatjon 259,
260,
296/88-28-01
was
issued
to
document the licensee's
failure to maintain configuration control.
During, the
licensee's
subsequent
evaluation
of the event it was
determined
that
no report to the
NRC was required per 10 CFR 50.72
or 10 CFR 50.73.
The licensee's
basis for this conclusion
was that
no Technical
Specifications
were violated
and that the hydrostatic
testing
was
not
normally
performed
during
power
operations.
However,
10 CFR 50.73 (a)(2)(v) requires
that the 'licensee
report
any
event
or condition that
alone
could
have
prevented
the
fulfilment of a safety function needed to mitigate the consequences
of
an
accident.
In this
case all four
DGs would have
overheated
when called
on to perform their function.
During discussions
held
with the
licensee
the
inspector
was
informed that
an
LER would
be
submitted.
The
licensee
subsequently
submitted
LER 296/88-,007
dated
December
30,
1988,
to
cover
the
event.
This
LER
was
classified
by the licensee
as
an voluntary informational report and
submitted approximately three
months after the event occurred.
The
NRC inspector
determined
that
a violation did occur, i.e.
the
licensee
failed to report the event to the
NRC within 30 days
as
required
by 10 CFR 50.73.
Violation 259,
260,
296/89-27-03
was
subsequently
issued
by the
NRC
for three
separate
examples
of the licensee's
failure to submit
a
required
LER in
a timely matter.
Since this failure constitutes
another similar failure, it will be included
as
a fourth example of
Violation 89-27-03.
The unresolved
item is therefore
closed
and any
corrective actions will be followed as part of the violation.
This
item is closed.
(CLOSED)
URI 259,
260,
296/88-33-03,
Unauthorized,
Undocumented
and
Inadequate
Maintenance Activity.
This
item
involved
a field observation
by
a
NRC inspector
of
fasteners
that
displayed
improper thread
engagement
on
a bolted
flange connection
.
The work on the connection
was later found to
have
been
performed
by an improper expansion of scope of an existing
maintenance
request
that
was being worked in the
same
area.
When
notified by the
NRC, the licensee initiated
CARR
BFP 881020
which
documented
the conditions.
TVA corrected
the fasteners
by replacing
them with bolts
of the
proper
length.
Work was
performed
by
maintenance
request
A803275.
TVA investigated
the occurrence
to consider if this type of improper
work control
was
a trend.
This effort involved use of the
CARR
trending
program.
The results indicated
no trend existed
because
no
similar
occurrences
were
documented within the previous
6 months.
Corrective actions
involved training of maintenance craft personnel
in the
importance
of work scope
and control.
The apparent
poor
communication
between
the field craft and the work supervisor
(who
was contacted
prior to performing the additional work) was stressed
as
the
root
cause.
The
corrective
actions
are
considered
appropriate.
The
NRC inspector,
after review of
CARR Trending
and previous
NRC
documented
findings,
considers
no violation of
NRC requirements
occurred
and that this occurrence
was isolated
and not the result of
a programmatic deficiency.
This item is closed.
(CLOSED) URI 260/88-35-02,
Missed 'SBGT Surveillances.
This
item
involved
a
SBGT train
becoming
when
the
surveillance
period
required
by the
technical
specifications
had
expired.
The
item
was
considered
unresolved
at the
time the
inspection
report
was
issued
because
the operability status
of
redundant
trains of the
SBGT was not readily available.
Subsequent
investigations
by
TVA revealed
that
a
second train of
SBGT was
because
its onsite
power supply
was
not available
(DG
B
was inoperable).
Mith two of the three
SBGT trains
the requirements
for
secondary
containment
stated
in
TS 3.7.B. 1.b
were
not
met.
Secondary
containment
was required for ongoing fuel pool activities
(Ref.
TS
3'.C.4).
This
event
was
reported
as
an operation
prohibited
by
TS in
Revision
1.
The information provided in the
LER is the
basis for resolving
URI 260/88-35-02
and concluding that a violation
of
NRC
requirement
did occur.
This
URI is considered
closed
and
upgraded to a licensee identified violation.
The
violation,
259,
260,
296/89-35-03,
is
considered
a
.
licens'ee-identified
violation
and
is
not
being
cited
because
criteria specified
in section
V.G. 1 of the
NRC enforcement
policy
were satisfied.
TVA investigation of the events
indicated that when SI 4.2.A-12 was
performed
on
November
29,
1988,
the
SI steps
associated
with train
"C" were
marked
N/A as
allowed.
The
SOS
acknowledged,
by his
signature
on the SI that acceptance
criteria were incomplete.
The SI
scheduling
section
identified the
need for train "C" testing'nd
placed
the
item on
a schedule
requiring performance prior to fuel
load.
The
impact
on the operability of the
SBGT was not effectively
passed
on to the operating shifts.
TVA attributed this to a lack of
a
formalized
process
for tracking the inoperability status
of
equipment for which SI's
had been partially completed.
The corrective
actions
taken
by
TVA was to develop
a formalized
process
for documenting
and tracking the operability status
of TS
required equipment.
22
This program
process
consisted
of revising the procedure
describing
the
conduct
of testing
(PMI-17. 1)
to
provide
directions
for
documenting
the conditions that prevent
the. completion
of'
SI and
ensuring that the
SOS
and the
STA are notified.
The
STA would then
be required to enter the condition in the
LCO tracking system.
PMI-15. 10,
"Tracking of Limiting Conditions for Operations,"
was
developed
and
implemented
to assist
the
SOS with the tracking of
components.
The
NRC inspector
reviewed
the corrective
actions
and
determined
that
the
concepts
and
program
were
adequate
and
implemented
in a
timely manner
and should prevent
a recurrence
of the event.
(CLOSED)
259,
260,
296/89-08-03,
Loss
of
Approximately
200,000 Gallons
From the Condensate
Mater Storage
Tank.
This
item involved
an event which occur red
on February
10,
1989,
during which the level of the Unit 1 condensate
storage
tank dropped
from
an indication of 26.7 feet at 4:00
a.m.
to
an indication of
10. 1 feet at 7:30 a.m..
This corresponded
to a loss of approximately
200,000
gallons
of water
in 3.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />.
Although the release
of
water
was
not monitored,
the activity was within 10 CFR 20 limits.
This loss of water
was not acted
upon until the evening of the
same
day, indicating
a lack of awareness
of the status of plant systems
by the control
room personnel.
The failure to adequately
maintain
an
awareness
of plant
systems
status
is considered
a violation of
plant
procedure
PMI-12. 12,
Conduct
of Operations,
section
4.3,
"Shift Personnel
Conduct," which states:
The operator
at the controls
and the immediate supervisor
must
be
continuously
alert
to plant
conditions
and activities
affecting plant operations,
including conditions
external., to
the plant
such
as grid stability, meteorological
conditions,
and
change
in support equipment status;
operational
occurrences
should
be anticipated;
alarms
and off-normal conditions
should
be
promptly
responded
to;
and
problems
affecting reactor
operations
should
be corrected in a timely fashion.
This failure to follow procedures
is identified
as Violation 259,
260, 296/89-35-04,
Failure
to
Respond
in
a
Timely
Manner
to
Off-Normal
Conditions.
An
NRC
NOV will be
issued
rather
than
. classifying it
as
'licensee
identified" with
no
NOV since
the
violation
was self disclosing.
The unresolved
item
URI 259,
260,
296/89-08-03 is closed
and upgraded to a violation.
(CLOSED) URI 259,
260, 296/89-11-02,
Single Failure Criteria.
This
item
involved
the
TVA design
control
process.
The
NRC
I
P
23
inspectors
concern
arose
over
the fact that several
single failure
criteria violations
in areas
of mechanical,
electrical, civil and
I8C design
had
been identified by Restart Testing
and other
means in
recent
months.
TVA investigated
each
issue
and
several
CA(Rs
resulted.
Corrective actions
or suitable
compensatory
measures
were
proposed for each
case.
t
CARR
BFT 880186
provided
a discussion
of the root cause
and the
recurrence
control
program for identification of single failure
deficiencies.
In the root cause
analysis
of the
CARR, several
conditions
adverse
to quality
had
been
identified concerning failure to meet single
failure criteria as identified below:
SCRBFNNEB8604 - Loss of 250VDC Battery
BD 2 Causes
Loss of
Three
U-3 Core Spray
Pumps.
SCRBFNNEB8607 - Loss of 250VDC Battery Concurrent with Recirc
Discharge
Break Results in Only One
Loop.
SCRBFNEEG8654 - Loss of Paralleled
Diesels 1/2
D 8
3D Causes
Loss of SBGT Trains
B 8
C (Common to all
units).
SCRBFNNEB8612
Loss of ECCS Division I Inverter Power to ATU
Causes
Loss of Automatic Vacuum Relief of
Torus.
NCRBFNMEB8403 - Loss of Offsite Power Concurrent with an
Accident Signal
Causes
Loss of Control
Bay
HVAC.
CA(R BFP880067 - Loss of 250VDC Battery
BD 1 Causes
Loss of
480VAC Load-Shed
Signals to Both U-1 480V Shut
Down Boards
and
Loss of Core Spray
Loop II.
CA(R BFP880154D01,
D02,
D03 - Certain Battery Failures
Concurrent
With
a
LOP/LOCA
Results
in Inadequate
Combination
of RHR Pumps.
These
deficiencies
were
identified
as
a failure to
have
an
appropriate
design
control
to
ensure
compliance
with the single
failure criteria specified in the
FSAR.
The
TVA Design Control
Program
was
a basic
issue that lead to the
development
of the
design
baseline
verification
program.
The
applicability of single fai lure criteria
was
addressed
by the
DBVP
and
is
discussed
for each
system
in the
system's
Design
Basis
Document.
This
increased
visibility of
such
a
fundamental
consideration
currently provides
an
acceptable
action
to prevent
recurrence.
24
The
items identified thus far were early designs
performed
before
enhanced
programs
were developed.
TVA provided the
NRC
a copy of its Single Failure
Design Criteria
Document
(BFN-50-729)
used
in the analysis
of the design of fluid
and mechanical
systems
and subsequent
design
changes.
This document
was
developed
to promote
a general
understanding
of single failure
requirements
'and
was
issued
in June
1987
as part, of the
DBVP.
The
inspector
considers
the
actions
taken
by
the
licensee
to
be
appropriate.
A violation for failure to implement
adequate
design
controls required
by 10 CFR 50 Appendix B, Criterion III is not being
cited
becaus'e
the criteria specified in section
V.G. 1 of the
NRC
Enforcement Policy were satisfied.
This
(NCV 259,
260,
296/89-35-05)
requires
no response.
The
inspectors
will continue
to monitor
TVA activities in this area.
URI 259,
260, 296/89-11-02 is closed.
(CLOSED) VIO 260/84-34-03,
Core Spray Relief Valves.
This violation involved the failure to test
the
Core
Spray
System
suction
relief
valves
per
ASNE
code
subsection
IWV-3510
requirements.
The
violation
was- previously
discussed
in
NRC
inspection
report
89-19
where
corrective
actions
by the licensee
regarding
ASME Testing
were
found satisfactory
and
documented
therein.
The issue
was not closed at that time because
a
CARR was
open
that
identified
concerns
related
to
improper relief valve
sizing.
TVA Site
Licensing
provided
the
NRC with documentation
that the
relief valve sizing
issue
had
been satisfactorily resolved.
The
resolution
involved calculations
of actual'ystem
flow requirements
to ensure
existing relief capacity
was adequate.
The system vendor,
GE,
concurred with the licensee.
Calculations,
GE correspondence,
and other documentation
were
reviewed in the
CA(R 88-07-69 closure
package
and were found complete.
This violation is closed.
(Open)
VIO 296/85-13-01
Failure to
Shut
Down With
Two Reactor
Protection
System Water Level Instruments
Following
a
NRC inspection
conducted 'to determine
the circumstances
surrounding
the inoperability
of two Unit 3
RPV water level
instruments
(LIS-3-203 A,
B) during
a reactor startup
on February
13,
1985, it was determined
that the responsible
licensee
personnel
failed to
commence
a reactor
shutdown in accordance
with required
actions
stated
in Technical
Specification
3. 1 (Table 3. 1.A).
T.S.
3. 1 states
there
shall
be
two operable
or tripped
systems
for
each trip function.
If the
minimum number of operable
channels
per
trip system
cannot
be
met for both trip systems,
the licensee
shall
initiate insertion of operable
control
rods
and complete insertion
of all operable
rods within four hours.
Even though there existed
sufficient redundant
information which should
have alerted operators
that
two required water level switches
were inoperable,
the licensee
did not shut
down
and continued
power escalation.
The reactor
was'
0
25
eventually
shutdown
on
March
9,
1985
to
conduct
further
investigations
required
by
TVA management
following review of the
-circumstances
associated
with the event.
This resulted
in the
NRC
issuing
a
severity
level II violation with
a civil penalty
(EA-85-13).
The inspector
reviewed
the
licensee's
responses
to the violation
and civil penalty
dated
August 21,
1985
and August 30,
1985.
In
that
response
the licensee
has
stated their inability to determine
explicitly the root cause
for the observed
level mismatch which led
to the
event.
It is suggested
that the level
mismatch
was
most
likely caused
by
a loss. of water. in the
"A" instrument
reference
leg.
Two possible
causeh
are
as follows:
Reference
level
leakage
via identified transgranular
stress
corrosion
cracking
in the line that existed
adjacent
to the
X-28 drywell penetration.
This
cracking,was
found during
post-event
investigation
and
repairs
have
been
made
to the
affected line.
Potential
for the presence
of air bubbles in the "A" reference
leg.
This possibility is
supported
by licensee
engineering
calculations
and
may
have
been
enhanced
by the
above listed
cause.
The presence
of high points in horizontal
runs
and the
number
and character
of restrictions
gives credibility to this
possibility.
Additionally, various activities affecting vessel
water level
and negative pressures
maintained
on the vessel
for
several
days prior to the startup could have contributed to the
introduction of air in the horizontal
runs of the reference
leg
lines.
The licensee's
analysis
of operator actions
pointed, out the
need for
additional
training
in diagnosing
water
level
instrumentation
problems
at off-rated conditions.
A similar condition
had existed
- during
an earlier startup that occurred
on
November
20,
1984
when
operators
also failed to diagnose correctly and fully appreciate
the
condition.
The
inspector
reviewed
'the
licensee's
corrective
actions
for
this violation.
Specifically, the following corrective actions
were
noted:
Both of the
above potential
hardware
problems
should
have
been
corrected
by completion of
ECN E-2-P7131.
This
ECN is related
to
Item II.F.2,
and relocated
the vertical runs of
reference
legs
outside
of the drywell
so
as to minimize the
potential
of erroneous
level
indications
resulting
from the
post-accident
environment
in the
drywell ~
This modification
was
completed
by
TVA during the
second
half of 1988
and is.
covered
in
more
detail
in
NRC
IR 88-32.
The
inspector
noted that during the
ongoing work gC inspection
was included
to verify instrument
line slope criteria were satisfied
and
that the presence of,high points in any horizontal
runs should
not be
a problem.
The
inspector
reviewed
documentation
including
memoranda
and
training
department
lesson .plans
associated
with classroom
and
simulator training.
Lesson
plans included training on the types
and
design
of the
available
level
instruments,
and their
expected
response
during
normal,
off-normal
and accident
conditions.
This
completed
licensee
training was provided to operators,
management,
and
and
was
intended to enable
them to more rapidly diagnose
water
level indication problems.
Additional training as part of the
planned start-up training program will cover the
same
subjects
and
is scheduled
to be completed
by December
22,
1989.
=The
inspector
examined
copies
of, training records;
a manager
of
licensing
memorandum
dated
March 21,
1989
(R08 890321 878);
and
Site
equality
Surveillance
Monitoring Report
dated April 14,
1989,
(R22
890414
973).
The monitoring report
was
conducted
by the
licensee
to
independently
verify. closure
of the
commitment
to
provide the training.
The
inspector
reviewed
the
licensee's
Unit
2
Operational
Readiness
Review Interim Report
dated
June
9,
1989.
This review
performed
by licensee
corporate
management
was the first of a two
phase
assessment
of the
readiness
of Browns
Ferry for restart.
Section VI.d covered
reactor vessel
water level
and included various
identified deficiencies
some of which are
as follows:
Interviews with operators
and
STAs indicated
an inconsistent
understanding
of what
was
entailed
in the
reference
leg
modification.
Documented
training
to
operators,
STAs,
and
management
to
enable
them to more rapidly diagnose
level indication problems
did not adequately
cover
the
new water level
reference
leg
installation.
Post modification testing did not verify proper function of the
modified system.
The acceptance
criteria
band specified in the post modification
test
equated
to approximately
27 inches of water.
Significant
indication errors
such
as
trapped air would not
be
cause
for
rejection.
Site licensee
management
has
not yet responded
to this review.
Due
to the significance of the
above
licensee
identified deficiencies
and
the
apparent
inconsistencies
between
these
comments
and the
documentation
provided
by site licensee
personnel,
this item will
remain
open pending further review.
(CLOSED)
296/86-06-06,
RHR/RHRSW/Diesel
Generator
'Inoperability.
This violation resulted
from
a
personnel
error of failure to
recognize
the inoperability of redundant safety systems.
One system
27
was
due to
an ongoing surveillance test
and the
second
system
was
made
when its associated
diesel
generator
was
removed
from service for scheduled
maintenance.
The combined affect
of these
out of service
systems
was
a reduction of RHRSM systems
to
less
than that
required
by the
TS for the
then
current plant
conditions.
TVA identified this violation and reported it in LER 296/86-04.
The
NRC considered
this occurrence
as
unnecessary if corrective action
from
a previous violation (84-26-02)
had been properly implemented.
The
NRC therefore
issued
a
NOV.
'VA responded
to the
NOV in a letter to the
NRC dated
May 1,
1986
and detailed
the corrective actions for the violation.
The
inspector
reviewed
the
TVA compliance
section
documentation
of the
followup and
closeout
of the plant's activities for this
violation.
The
package
was thorough
and
complete.
All corrective
action
commitments
were
found to have
been
completed.
Corrective
actions
included clarification of TS 3. 0. 5
as it applies
to cold
shutdown
conditions
and
development
of shift turnover checklists.
This violation is considered
closed.
(CLOSED) VIO. 259,
260, 296/87-14-02,
CREV Train
B Inoperable.
This violation involved the
CREV system
and the fact that the system
was
determined
to
be
because
air
flow rates
were
inadvertently
set
below the
minimum allowed
by the
TSs.
This
violation
was
discussed
previously
in inspection
report
89-19.
In that report the licensee's
corrective actions
were
reviewed
and
several
a'spects
of the violation were closed.
The following items
were not closed at that time:
1)
The results
of special test
ST 8726 designed to analyze
systems
flows in various
damper line-ups indicated that the
CREV system
flowrates
could
exceed
the
TS
maximum allowable with certain
damper alignments.
2)
The
system
did not meet the design
content of the
because
significant unfiltered
inleakage
of outside air into
the control
room habitability zone bypassed
the system.
3)
The
acceptance
criteria of the
TS Surveillance
Instructions
could
be met satisfactorily
even
though the
system
would not
perform its intended function because
of unmonitored inleakage.
4)
The related
issue
of the effect of toxic chemical
releases
from accidents
on transportation
routes
near the site did not
appear to meet requirements
of R. G. 1.78.
These
complex
issues
addressing
the ability of the
CREV system to
maintain
the control
room habitability during accident
conditions
has
been
under consideration
by the
NRC and
TVA for a long period of
time.
28
Recent actions
on the remaining items are
as follows:
1)
After *a
review of special
test
8726,
flowrates
were
determined
by the
NRC inspector to
be within TS limits.
This
determination
was
reached
after discussion
with ventilation
system
engineers
and analysis
of test results
summary.
This
item is considered
closed.
2)
The fact that
the
system
does
not
meet its
intended
function
is
the
specific
topic of
an
amendment
request
submitted
by
to
the
NRC
in
a
letter
dated
February
14,
1989.
The
change
request
number
265T discusses
in
detail
the deficiencies
of the
system
design
and operation.
Approval of the
change
request or other action will be required
before
Unit 2 startup
to resolve
the
CREV system operability
issue.
3)
The fact that
a
TS surveillance instruction assumes
that system
integrity had
once
been
established
is an acceptable
practice.
The
then verifies that
major
components
of that
system
continue
to
function
as
designed
and
other administrative
programs will preserve
system structural
configurations.
These
programs will ensure
that
system
performance will not degrade
unknowingly.
The
NRC inspector
has
determined after
review of
the
system
surveillance
program
that it meets
TS
requirements
as
well
as industry standards
and is considered
satisfactory for this item to be closed.
4)
The issue of toxic gas
releases
near the site was discussed
in
a letter
from TVA to the
NRC dated
June
27, 1989.
In summary,
that letter stated
that
TVA concluded
that the plant
meets
as it applies
to
Browns
Ferry Toxic
Gas
Analysis.
The
discussion
within the letter directly
and
clearly addresses
the
NRC concerns.
Resolution of this issue
now rests
with the
NRC.
Since the scope of this issue
exceeds
the
scope
of the original violation and is clearly documented
in the
June
27,
1989 letter,
the
NRC inspector
considers
the
violation regarding
CREVs testing
techniques
as
closed.
This
is not
an acceptance
of the control
room toxic gas analysis
or
habitability issue.
This violation is closed.
(CLOSED)
VIO 259,
260,
296/88-18-02,
Failure to Initiate a CA(R for
the Overloaded
1/2
D DG.
This item involved
a personnel
error leading to
an overload of the
Units 1/2
D
DG which occurred
during
a conduct of a special
test
ST 88-09
in June,
1988.
The
craftsman
was
taking
a reading to-
verify
a
parameter
being
monitored
on
a recorder.
The
actual
over load condition lasted for approximately
30 seconds.
However,
as
a result
of the
event,
no
CARR
was initiated. 'he
inspector
reviewed
SDSP 3.7,
"Correction Action," and
SDSP
3. 13, "Corrective
29
Actions"
and
noted that both procedures
outline activities required
when
CA(Rs are initiated, reviewed,
and closed out..
SDSP 3.7 states
the following in subsection
6. 1. 1:
Confirmed degradation,
damage,
failure,.'alfunction,
or loss of
plant,.structures,
systems,
and
components
that could adversely
affect
the
performance
of
a safety-related
function (i.e.,
nonconformance).
This
would include
but not
be limited to
material
failure,
abnormal
or
unexpected
wear,
manufacturer
defects,
fai lure
to
function
as
intended,
and repetitive
failures.
SDSP 3. 13 states
the following in subsection
6.2.1.F:
Items
which have
been
subjected
to conditions for which they
have
not
been
designed,
unless
done
intentionally
by
an
approved
and
properly
authorized
procedure
such
as
overpressure,
overvoltage,
overheating,
overstressing,
or
environmental
conditions
hazardous
to their function.
This
appears
to
be
an
inconsistency
in
. that
SDSP 3.7 indicates
Confirmed
Damage,
whereas
SDSP
3. 13 indicates
Condition for Which
They
Have
Not Been Designed.
Both SDSPs
are in effect as of the end
of this reporting period.
The
NRC inspector further noted that
SDSP 3.7,
section
2. 1 states
the following:
CARR's initiated
on or after August 16,
1988, shall
be processed
in accordance
with
SDSP
3. 13, Corrective Actions.
The
NRC inspector
also
noted that
SDSP
3. 13, initial revision was dated
August
5,
1988
and that
any future
occurrences
of
a system
or
component
being subjected
to conditions for which they have not been
designed will be initiated
and processed
in accordance
with
SDSP
3. 13.
This item is closed.
4.
Exit Interview (30703)
The inspection
scope
and findings were summarized
on August 16,
1989 with
those
persons
indicated in paragraph
1 above.
The inspectors
described
the
areas
inspected
and
discussed
in detail
the
inspection
findings
listed below.
The licensee
did not identify as proprietary
any of the
material
provided
to
or
reviewed
by
the
inspectors
during this
inspection.
Dissenting
comments
were not received
from the licensee.
Item
Descri tion
259,
260, 296/89-35-01
259,
260, 296/89-35-02
259,
260, 296/89-35-03
IFI, Flexibility of Reactor Water Level
Sensing
Lines, paragraph
3.g.
IFI, Storage of gA Records,
paragraph 3.l.
in a
TS Violation,
paragraph
3.s.
30
259,
260, 296/89-35-04
259,
260, 296/89-35-05
Violation.
Failure to Respond
in a Timely
Manner
to=-
Off-Normal
Conditions,
paragraph 3.t.
NCV, Design Control of Single Failure,
paragraph
3'.
ASOS
ATU
BF
BFNP
CAQR
CHRRM
DBVP
DCN
GL
IEB
IEEE
IFI
IM
IR
KV
LCO
LER
LIV
LOP/LOCA
MMI
NPRD
NRC
,Ql)
American Society of Mechanical
Engineers
Assistant Shift Operations
Supervisor
Analog Trip Units
Browns Ferry
Browns Ferry Nuclear
Power
Plant
Boiling Water Reactor
Condition Adverse to Quality Report
Containment
High Range Radiation Monitors
Control
Room Emergency Ventilation System
Design Baseline
and Verification Program
Design
Change Notice
Design
Change
Request
Diesel Generator
Engineering
Assurance
Emergency
Core Cooling Systems
Engineering
Change Notice
Emergency
Equipment Cooling Water
Engineered
Safety Feature
Final Safety Analysis Report
General
Electric
Generic Letter
High Pressure
Coolant Inspection
Heating, Ventilation,
8 Air Conditioning
Impact Evaluation
Inspection
and Enforcement Bulletin
Institute of Electrical
and Electronics
Engineers
Inspection
and Enforcement
Report
Inspector
Followup Item
Intergranular Stress
Corrosion Cracking
Instrument Maintenance
Inspection
Report
Intermediate
Range Monitor
In Service Inspection
Ki 1 ovolt
Limiting Condition for Operation
Licensee
Event Report
Licensee Identified Violation
Loss of Power/Loss of Coolant Accident
Motor Generator
Mechanical
Maintenance Instruction
Non-cited Violation
Nuclear Plant Reliability Data System
Nuclear Regulatory
Commission
Preventive
Maintenance
0
31
PMI
RHRSM
SDBD
SDSP
SOS
TS
ater
Plant Manager Instruction
Quality Assurance
Quality Control
Raw Cooling Mater
Residual
Heat
Removal
Residual
Heat
Removal Service
W
Reactor Protection
System
Reactor
Pressure
Vessel
Restart Test Program
Standby
Gas Treatment
System
Shutdown Board
Site Director Gtandard Practice
Safety Evaluation
Surveillance
Instruction
Service Information Letter
Shift Operations
Supervisor
System Pre-Operation
Checklist
Sequoyah
Nuclear Plant
Source
Range Monitor
Shift Technical
Advisor
Test Exception
Three Mile Island
Technical Specifications
Valley Authority
Unresolved
Item
Violation
0
0