IR 05000259/1998004

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Insp Repts 50-259/98-04,50-260/98-04 & 50-296/98-04 on 980524-0711.No Violations Noted.Major Areas Inspected: Aspects of Licensee Operations,Engineering,Maint & Plant Support
ML18039A470
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 08/07/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18039A469 List:
References
50-259-98-04, 50-259-98-4, 50-260-98-04, 50-260-98-4, 50-296-98-04, 50-296-98-4, NUDOCS 9808180103
Download: ML18039A470 (54)


Text

U.S.

NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

License Nos:

50-259.

50-Z60.

50-296 DPR-33, DPR-52, DPR-68 Report Nos:

50-259/98-04, 50-260/98-04 '0-296/98-04 Licensee:

Tenn'essee Valley Authority Facility:

Browns Ferry Nuclear Plant, Units 1. Z, 8 3 Location:

Corner of Shaw and Browns Ferry Roads Athens, AL 35611

Dates:

Inspectors:

Hay 24, 1998 - July. 11.

1998 L. Wert, Senior Resident Inspector J. Starefos, Resident Inspector E. DiPaolo, Resident Inspector E. Testa, Reactor Inspector (Section Rl)

Approved by:

H. 0. Chri stensen, Chi ef Reactor Projects Branch

Division of Reactor Projects 9808180103 980807 PDR ADOCK 05000259

PDR Enclosure

EXECUTIVE SUMMARY Browns Ferry Nuclear Plant, Units l. 2,

& 3 NRC Inspection Report 50-259/98-04.

50-260/98-04 '0-296/98-04 This integrated inspection included aspects of licensee operations.

engineering, maintenance, and plant support.

The report covers a six-week period of resident inspection and inspection of Radiological Controls by a Region II Division of Reactor Safety Inspector.

~Qerati ons

~

The control room operators responded correctly to the tripped 3B recirculation pump and utilized a conservative approach regarding consideration of the power/flow conditions.

The licensee's use of thermography to assess damage to switchyard ceramic insulators was good (Section 01.1).

The licensee's failure to implement the procedure for returning a loop I Residual Heat Removal (RHR)

pump and heat exchanger to service in an operable loop resulted in an unrecognized entry into a more restrictive Technical Specification Limiting Conditions for Operation.

The licensee's corrective actions were adequate.

Core Spray and RHR procedures were enhanced to address a vulnerability while opening normally closed containment isolation valves (Section 01.2).

~ ~

General material conditions of the Unit 2 Core Spray System were considered good.

The inspector identified that numerous dust covers for GE type HGA relay.

used in various safety system electrical circuits, were not properly reinstalled flush with the cabinets.

The improperly installed covers did not pose an operational concern (Section 02.1).

Maintenance Test equipment was not set up properly and contributed to unnecessary troubleshooting delays in the calibration of the Reactor Core Isolation Cooling (RCIC) system governor.

Maintenance personnel were unfamiliar with test equipment operation although trained to perform the task.

Preliminary licensee investigation efforts were adequately focused on the issues that emerged during performance of the RCIC system governor calibration (Section Ml.1).

The prejob brief for the RCIC System Rated Flow at Normal Operating Pressure test was detailed and instrumental in successfully coordinating the performance of the various post maintenance tests performed during the surveillance.

The operator performing the time-to-rated-flow portion of the test demonstrated a good questioning attitude in questioning the acceptability of an'bnormal system valve lineup.

Control and supervision of the unit operator trainee was good (Section Ml.2).

~

A maintenance worker performed unauthorized work by adjusting valve packing without operations authorization.

Licensee corrective actions were considered good.

Additional motor operated valve testing was performed although not requi red by the as-found condition (Section Ml.3).

~

The licensee effectively performed corrective maintenance on a Unit 3 torus dynamic restraint that had a leaking oil reservoir.

The licensee maintained good control of contractor personnel performing the functional test of the torus dynamic restraint (Section M2. 1).

En ineerin

~

The correction coefficient (TAU) used to adjust the Operating Limit Minimum Critical Power Ratio (OLMCPR) for slow control rod scram insertion times was incorrect for several Unit 2 and 3 operating cycles, however, the corrected OLMCPR was never exceeded.

Weak design controls were in place between the licensee and the contractor performing core reload analysis.

The licensee corrective actions were prompt and complete (Section fl.l).

Plant Su ort

~

Radiological facility conditions in radioactive waste storage areas.

health physics facilities and Turbine and Reactor Buildings were found appropriate and the areas were properly posted and material appropriately labeled.

Personnel dosimetry devices were appropriately worn.

Radiation work activities were appropriately planned.

Radiation worker doses were being maintained well below regulatory limits and the licensee, was maintaining exposures ALARA.

A special team was aggressively planning the U3 drywell cleanup.

The Whole Body counting

'program was performed as procedurally required (Section Rl).

Re ort Details Summar of Plant Status Unit 1 remained in a long-term lay-up condition with the reactor defueled.

Unit 2 operated at or near full power with the exception of scheduled downpower activities.

Unit 3 operated at or near full power with the exception of a power decrease on June 27 due to the 3B recirculation pump motor generator trip (Section 01.1),

a power decrease on June 24, 1998.

when a switchyard problem caused voltage perturbations on the condensate demineralizer system (Section 01. 1).

and scheduled downpower and end of core life activities.

~l-tl ti

Conduct of Operations Ol. 1 0 erational Transients Affectin Unit 3 a.

Ins ection Sco e

71707 61726 The inspectors reviewed the licensee's actions to address two transients which aff'ected Unit 3 during the inspection period.

b.

Observations and Findin s At 5:48 p.m on June 27.

1998. the 3B recirculation pump motor generator tripped.

This placed Unit 3 in region 2 of Technical Specification (TS)

Figure 3.5.H-l.

The control room operators responded to the event and promptly initiated control rod insertion to exit region 2.

As of 6:07 p.m.,

power and flow conditions were such that region 2 had been exited.

The senior resident inspector responded to the site several hours after the incident and verified that the actions required by TS for single loop operations had been completed.

The inspector verified that plant conditions were being maintained clear of region 2.

The inspector examined completed Surveillance Instruction 3-SI-4.5.H. l.b, Core Thermal Hydraulic Stability Flow Decrease and noted that the power/flow conditions had been just on the edge of region 2.

Core flow was recorded as 45 percent of rated.

The operator actions were in compliance with procedures 3-AOI-68-1. Reci rc Pump Trip/Core Flow Decrease and 3-GOI-100-12A, Unit Shutdown for Power Operation to Cold Shutdown and Reductions in Power During Power Operations.

A 24-hour TS Limiting Condition for Operation (LCO) had been entered.

The recirculation pump motor generator set tripped due to a loss of field on the exciter.

Arcing had caused damage to the exciter brushes and brush holder assembly.

The licensee used parts from a Unit 1 motor generator set to replace the damaged equipment.

The inspector observed

that work order 98-007252-000 and procedure EPI-0-068-TST001.

Maintenance and Testing of the Recirculation M/G Sets and Associated Pump Motors, were present at the work site and being used during the work.

Numerous engineers were assisting with the recovery of the motor generator.

The recirculation pump was restored to operation on the afternoon of June 28.

1998.

On June 24.

1998, Unit 3 experienced voltage perturbations on the condensate demineralizer system that were caused by switchyard problems.

The Maury 500 kV line tripped and reclosed when a potential transformer device in the switchyard exploded.

Several adjacent ceramic insulators were damaged.

The licensee used thermography to assist in assessing the damage to some of the more severely affected insulators.

The voltage perturbations on Unit 3 condensate demineralizer system shutdown the programmable logic controllers.

This should have caused the effluent flow control valves (E-valves) for each demineralizer to lock in position; however, four of the vessels E-valves closed, isolating the vessels.

Low condensate booster pump suction alarms were received and power was decreased to compensate for the lower net positive suction head.

Unit 3 power was decreased to approximately 84%.

An additional demineralizer isolated and the resultant differential pressure across the vessels caused the demineralizer bypass valve to opens which relieved system differential pressure and cleared the booster pump alarms.

The licensee initiated a problem evaluation report to address the condensate demineralizer E-valve problems.

Conclusions 01.2 The control room operators had responded correctly to the tripped 3B

.recirculation pump and utilized a conservative approach regarding consideration of the power/flow conditions.

The licensee's use of thermography to assess damage to switchyard ceramic insulators was good.

Failure to Follow Procedure Durin Fill and Vent Ins ection Sco e

71707 The inspector reviewed the licensee's actions when operators did not use the correct procedure to fi11 and vent an inoperable portion of the Loop I Residual Heat Removal System (RHR).

In additions the inspectors walked down portions of the pressure suppression chamber (PSC)

head tank and supply piping to the RHR discharge and questioned the control of normally closed containment isolation valves from the condensate storage and supply system to the RHR discharge pipin Observations and Findin s On Nay 25, 1998, while veri fying that the RHR system was filled and vented following maintenance which affected the 3A RHR pump and heat exchanger, the licensee noted that the RHR loop discharge pressure dropped below the TS required pressure of 48 psig.

Upon further investigation, the licensee determined that discharge pressure had also decreased below the required minimum on the previous shift during fill and vent activities.

The licensee declared RHR Loop I inoperable and entered a 24-hour TS LCO.

The licensee documented the event in a problem evaluation report.

Discussions with the licensee indicated that the initial fill.and vent was performed while the tagout was being lifted and that the*operators did not use the appropriate procedure for fill and vent while returning a loop I RHR pump and heat. exchanger to service in an operable loop.

Specific guidance is available in Operating Instruction 2-0I-74.

Residual Heat Removal System, Section 8. 1.3.

The. operators did not recognize that this specific guidance was available and attempted to use other methods to fill and vent.

This procedure specifically cautioned the user that close coordination is required to prevent operable Core Spray(CS)

and RHR loops discharge pressures from dropping to less than 48 psig and that a TS LCO may result if discharge pressure is allowed to drop below 48 psig.

The operators also did not identify that the 7-day LCO for the out of service pump and heat exchanger had become a more limiting LCO when the pressure dropped below 48 psig and the loop became inoperable during the initial fill and vent.

Since this was recognized by the next shift during the subsequent fill and vent, and the LCO was entered including the time frame of the initial pressure drop, the allowed outage time for the LCO was not exceeded.

The licensee's corrective actions included each Shift Manager discussing this event in detail with his respective crew.

The involved Unit Supervisor wi 11 be required to prepare a presentation which will include the errors committed during this evolution, lack of meeting management expectations, importance of using proper documents, consequences of lack of awareness and sensitivity to the status of safety systems, and importance of adequate pre-job briefings.

The licensee's failure to implement the procedure for returning a loop I RHR pump and heat exchanger to service in an operable loop is a failure to follow procedure violation.

This non-repetitive, licensee-identified and corrected violation is being treated as a Non-Cited Violation, consistent with Section VII.B.1 of the NRC Enforcement Policy.

This non-cited violation is identified as 296/98-04-01, Failure to Follow Procedure for RHR Fill and Ven The inspector reviewed several previously recorded problems with LCO documentation.

Upon review. the inspector determined that the allowed outage time was exceeded in only one case.

That specific example was addressed as a severity level IV violation in NRC inspection report 259,260.296/97-10 (see section 08.4 for closure documentation).

The inspector determined that the root cause of the previous violation was not consistent with the cause of the current example and corrective actions for the previous violation would not have prevented the present violation.

While reviewing this event, the inspectors walked down portions of the PSC head tank and associated piping which maintains the RHR and CS system discharge piping full.

This PSC system supplies water to the system discharge piping through two IST tested check valves which perform the primary containment isolation function.

The condensate supply and storage system also supplies a source of water to the RHR and CS system discharge piping through normally closed manual isolation valves.

The inspector questioned the control of those valves and upon discussion with the licensee, it was identified that the normally closed valves were allowed to be opened by Operating Instructions OI-74.

Residual Heat Removal System and OI-75. Core Spray System while primary containment was required.

The licensee has enhanced the procedures to post an operator at the valve to close the valve if primary containment isolation is necessary.

In addition, the licensee is reviewing other procedures which may be affected by this vulnerability.

The inspector verified that this new guidance remained in the latest version of the Unit 2 and 3 OI-74 and OI-75 procedures.

Conclusions The licensee's failure to implement the procedure for returning a loop I RHR pump and heat exchanger to service in an operable loop resulted in an unrecognized entry into a more restrictive TS LCO.

The licensee's corrective actions were adequate.

CS and RHR procedures were enhanced to address a vulnerability while opening normally closed containment isolation valves.

02.1 Operational Status of Facilities and Equipment Unit 3 Core S ra S stem Walkdown Ins ection Sco e

71707 The inspector performed a detailed walkdown of the Unit 2 CS system.

The inspector reviewed the FSAR, TS, plant procedures.

and the Unit 2 Probabilistic Risk Assessment Individual Plant Examination system notebook for the CS system in preparing for the inspectio b.

Observations and Findin s General material conditions of the CS system appeared to be good.

No problems were found with the lineup of system valves, breakers.

switches or instrumentation.

While inspecting system instrumentation in the Unit 2 Auxiliary Instrument Room, on June 6.

1998. the inspector found that numerous dust covers for GE type HGA relays, used in various safety system electrical ci rcuits. were not fully inserted.

Closer examination of the relays showed that the covers were not installed properly.

These covers are removed by operations and maintenance personnel during system testing'nd maintenance.

When properly installed the dust covers are held in place with metallic retention springs located on the relay housing which clip into a recessed groove on the inside of the dust covers.

The dust covers were reinstalled with the retention springs wedged on the outside of,the covers.

This resulted in the covers not being able to be fully inserted.

Many of the retention springs were found to be broken off.

This may have been due to the stresses placed on the springs with the springs on the outside surface of the covers.

The inspector informed the licensee of this condition.

The licensee initiated a Problem Evaluation Report (BFPER98-006418-000).

The licensee-determined that the improperly installed covers did not pose an operational concern since they were not required for seismic support of the relays.

The inspector examined the interior of a sample of the ECCS instrumentation cabinets with the aid of an operator.

No broken retention spring parts were found inside the cabinets.

The inspector determined that, due to the equipment arrangement, no obvious problems would have resulted if the metallic retention spring parts fell in the interior of the cabinets.

Material conditions were generally good.

In one cabinet, part of a broken wire raceway cover was found resting on interior cabinet wiring and was removed by the operator.

Conclusion

08.1 General material conditions of the Unit 2 CS system were considered good.

The inspector identified that numerous dust covers for GE type HGA relay, used in various safety system electri.cal circuits, were not properly reinstalled flush with the cabinets.

'The improperly installed covers did not pose an operational concern.

Miscellaneous Operations Issues (92901)

Closed Violation 296/97-05-01, Failure to Reset Locked Scoop Tube.

This issue was reviewed in Inspection Report 259,260.296/98-03 and closed as 260/97-05-01.

This entry administratively closes the issue for Unit '

Closed Unresolved Item 260/97-010-02.

Technical Specification Requirements During Control Rod Drive (CRD) Accumulator Maintenance.

This item was unresolved pending additional review to ensure that regulatory requirements for inoperable CRD accumulators and entry into TS LCO were met.

The Unresolved Item addressed two major issues; operability of the CRD accumulators during normal operations when an accumulator low pressure alarm actuates, and operability of the accumulators during a previous Unit 2 work activity in which the accumulators were rendered inoperable (one at a time) for calibration of the pressure and level switches during operations.

Res onse to accumulator low ressure alarms:

The licensee closely reviewed the actions being taken on an accumulator low pressure alarm.

During review of related Problem Evaluation Reports (PERs)

~ the inspector noted that PER 970094 contained a technical evaluation that indicated that the control rod drive would be able to fulfillits safety function with accumulator pressures as low as 895 psig.

Since the low pressure alarm setpoint is greater than or equal to 940 psig, the control rods would usually be expected to perform their safety function with low pressure alarms provided that the accumulator remains above a specified minimum pressure.

However, licensee management has decided that the practice of declaring accumulators inoperable on low pressure alarms will continue.

The importance of completing the actions required by TS 3.3.A.2 such as.

evaluation to ensure that the rod is not within a 5X5 array of another inoperable rod, was emphasized to the operators.

In addition to the NRC inspector's observations that the 5X5 array requirements were not being rigorously reviewed with each inoperable control rod, the licensee's quality assurance had initiated Problem Evaluation Report 980045 addressing a similar issue. 'n recent months. the resident inspectors have noted that this particular factor is being evaluated by the operators during responses to accumulator low pressure alarms.

The operators are expected to declare the rod inoperable.

evaluate the 5X5 criteria, and initiate corrective actions.

The inspectors have observed that, in most cases'he low pressure alarm is cleared in less than

minutes.

Discussions with the NRR Project Manager and NRC management indicated that since there is not a specific time in which the actions to ensure shutdown margin are required to be completed, these actions were acceptable and in compliance with requirements.

Inspection Report

98-03 describes

NRC observation of recharging of two accumulators.

No

significant deficiencies

were identified.

The inspectors

noted that the Improved Standard

Technical

Specifications,

expected to be implemented in July 1998, contain more

specific guidance

on accumulator pressure

and operability of the control

rods.

Specifically,

an accumulator

can be inoperable for an hour before

the

CRD must be declared

inoperable.

Additional review was conducted

regarding the requirements

for'tracking

of TS LCOs.

Revision ll of Alarm Response

Procedure

(ARP) 2-ARP-9-5A.

Control

Rod Drive Accumulator Pressure

Low/Level High added specific

requirements

for entry into a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />

LCO and evaluating

5X5 array

requirements.

The ARP also specifically requires entries into the

operating

logs describing those actions.

The inspectors

have observed

that log entries

have

been

made to address all control rod inoperability

periods,

even before the

ARP contained specific requirements to do so.

(juality assurance

has completed

reviews focused

on logging of TS LCOs.

In recent

months,

no significant deficiencies

were identified.

Additionally, the inspectors

have found that the Unit Supervisors

are

consistently

aware of the

LCOs that the units are in.

The inspectors

concluded that the method of tracking the inoperable control

rods is

adequate

and meets regulatory requirements

for LCO monitori'ng.

Problem Evaluation Reports

have also been initiated regarding repetitive

low pressure

alarms

on

HCUs which were not addressed

by work requests

and other problems with the alarms.

The inspector

reviewed these

PERs

and concluded the corrective actions were adequate.

Calibration of Accumulator Pressure

Switches

Durin

0 erations:

The inspector

reviewed the work orders utilized for approximately

switch calibrations

performed during the period September

21 to

September

24.

1997.

The work was performed

on one control rod hydraulic

control unit at

a time with the reactor

at power.

Each work order

contained appropriate

precautions

and referenced

approved

procedures

for

the work.

Review of log entries indicated that typically, the

LCO for

an inoperable control rod was entered for about

15-20 minutes to

complete the work.

No single accumulator

was inoperable for greater

than

one hour.

Standard

Program

and Process

(SPP)

-7. 1,

Work Control Processes.

approved in January

1998. contains

guidance

r egarding risk assessment

for on-line maintenance activities.

The inspector

noted that Section

3.2. 1 contains

some guidance

regarding recurrent entry into a

LCO for

multiple activities.

SPP-7. 1 replaced Site Standard

Practice

SSP-7. 1.

The inspector

reviewed the revision of SSP-7. 1 in effect at the time

that the work was performed.

SSP-7. 1 did not contain

a discussion

regarding

multiple LCO entries.

Browns Ferry implements the SSP-7. 1 schedule risk assessment

through

Technical Instruction O-TI-167,

BFN Dual Unit Maintenance.

The Control

Rod Drive pumps are listed on the maintenance

matrix but the hydraulic

control units are not since the. matrix does not address

specific plant

equipment at that level.

The inspectors

concluded that no regulatory requirements

were violated

during the maintenance activities

on the accumulators.

The above review

indicates that the licensee's

actions in response

to accumulator

low

pressure

alarms were reasonable

and met regulatory requirements.

Throughout the reviews of this item, the inspectors

did not identify any

accumulator

pressures

that were low enough to affect the control rod

safety function.

The licensee

has indicated to the inspectors that in

the future. it does not intend to schedule

routine calibration of

accumulator switches during power operations.

The unresolved

item is

closed.

Closed

Licensee

Event

Re ort

LER 296/97-004-00.

Unplanned

Manual

Start of an Emergency Diesel Generator

During a Scheduled

Redundant

Start Test.

A control

room operator failed to meet management

expectations

regarding touch Stop.

Thinks Ask, Act. and Review (STAR).

The operator turned

away from the control panel to verify a 'procedure

step

and did not re-perform verification that he was on the correct

switch.

The inspectors

have observed that management

has continued to

emphasize correct implementation of self-checking

and verification

activities since this incident.

Incorrect switch manipulations

by

control

room operators

have been rare at Browns Ferry in recent years.

The inspectors

have observed that overall implementation of these

actions

has continued to be more consistent.

For example,

Inspection

Report 98-03 contains

several

positive observations

of self-checking

and

verification actions during specific evolutions.

The inspectors

have

also noted that the emphasis

on these techniques

during training

sessions

has also been strengthened

in recent

months by management.

This

LER is closed.

Closed

Violation 296/97-10-03,

Failure to Complete

TS Action for

Inoperable

Containment Isolation Valve.

This violation involved the

failure to complete

a

TS action for

a containment isolation valve.

The

licensee

responded to this violation in a letter date

December

23,

1997.

The licensee

determined that the root cause of the violation was that

the operations

crew lacked

a questioning attitude.

The Senior Reactor

Operators

(SROs)

developed

a mind-set regarding the failure mechanism

for the valve problems

and did not fully assess

new information for the

effect on TSs.

The licensee

performed sensitivity training with the

SROs

on

LCO entries

and methodology during troubleshooting.

This

violation is close II. Maintenance

Conduct of'Maintenance

Reactor

Core Isolation Coolin

Governor Control

S stem Calibration

Ins ection Sco

e

62707

37551

The inspector

observed

portions of performance of ECI-0-071-GOV001.

Reactor

Core Isolation Cooling (RCIC) Governor Control System

Calibration.

Assistance

in troubleshooting efforts by engineering

personnel

were also observed

when unexpected

results

were obtained

during calibration performance.

Subsequent

Incident Investigation

Team

activities were also reviewed.

Observations

and Findin s

On June

23, the Unit 2 RCIC system

was taken out of service for

scheduled

maintenance.

modifications,

and testing.

On June

24. the

inspector

observed

the performance of portions of the governor control

system calibration.

The RCIC governor calibration is performed by removing the normal

turbine inputs to the governor

and connecting'xternal

test equipment to

simulate turbine conditions.

Governor output voltage is measured.

compared to acceptance criteria and adjusted if necessary.

Problems

were encountered

during system static calibration testing.

RCIC turbine speed

(using

a sine wave generator)

and

pump flow (using

a

DC current source)

were used to simulate operation at low speeds.

Output voltage was expected to be relatively stable,

however,

a

fluctuating output was observed.

The fluctuations were first believed

to be indicative of the need to adjust the governor settings.

The

inspector questioned

the setting of the sine wave generator

voltage.

The procedure called for an output voltage in AC volts root mean square

(RMS).

However, the display on the instrument

appeared to be set

on

peak-to-peak

voltage.

The electrical

mechanics

attempted to change

output voltage function of the sine wave generator

and were unable to

obtain

an

RMS voltage readout.

The electrical

mechanics

then adjusted

output voltage to read the required value as measured

by a portable

digital voltmeter.

This action resulted in an output voltage that was

closer to the required output but did not resolve the voltage

fluctuations*.

Additional troubleshooting

was later performed

by a team of engineering

and maintenance

personnel.

The team initially bel,ieved that the problem

with the fluctuating output voltages

was due to the removal of a wire

lead on

a governor terminal

when installing the test equipment.

This

troubleshooting effort did not resolve the fluctuating output voltage.

After consulting the technical

manual

for the sine wave generator,

which

was not originally present at the job site. the troubleshooting

team

found that the initial settings for the sine wave generator

were

incorrect (i.e., sine wave voltage offset and wave symmetry).

Removal

of these functions alleviated the voltage fluctuations.

The inspectors

reviewed the training requirements

for maintenance

personnel

to perform. the governor calibration.

The inspectors

found

that the personnel

involved with the task

had completed the training.

The licensee initiated

a

PER due to the problems encountered

during RCIC

testing.

The licensee

appointed

an Incident Investigation (II) team to

evaluate

the

RCIC testing.

This was due to the similarities of the

problems encountered with past problems during testing of the High

Pressure

Coolant Injection system

(see

M1.4 of IR 97-05)

and the Standby

Gas Treatment

system

(see Ml. 1 of IR 98-02).

At the end of the inspection period the II team had not completed their

review.

The inspector

reviewed the preliminaries findings of the team.

Some of the more significant findings were as follows:

~

The maintenance

workers were trained with test equipment that was

different than that used during the

RCIC governor calibration

surveillance.

~

Knowledge retention

by the personnel

performing the RCIC governor

calibration

may not have

been sufficient due to the time interval

between training and task performance.

Some of the maintenance

workers were found to have been trained

on the task performance

several

years prior to actual

performance.

Due to the similarities of the maintenance

and test equipment

problem

encountered

during this RCIC system governor calibration

as

compared

with past problems, this is identified as

an Inspection.Follow-up Item

(IFI) 260,296/98-04-01,

Use of Maintenance

and Test Equipment.

This IFI

wi 11 focus on the use of maintenance

and test equipment during the

performance of maintenance

and surveillance activities.

c.

Conclusion,

Test equipment

was not set

up properly and contributed to unnecessary

troubleshooting

delays in the calibration of the

RCIC governor.

Maintenance

personnel

were unfamiliar with test equipment operation

although trained to perform the task.

Preliminary licensee

investigation efforts were adequately

focused

on the issues that emerged

during performance of the

RCIC system governor calibration.

RCIC S stem Rated

Flow at Normal

0 eratin

Pressure

Ins ection

Sco

e

71707

61726

The

inspector

observed

the performance of the Unit 2 RCIC system flow

rate surveillance.

The testing

was performed in order to return the

syst'm to operable status

following a period of preventive

and

corrective

maintenance.

Observations

and Findin s

On June

25 and 26,

1998, the inspector

observed the performance of 2-SI-

4.5.F. 1.d,

RCIC System Rated

Flow at Normal Operating Pressure.

This

test is periodically performed to demonstrate operability of the

RCIC

system in accordance

with TS.

The test

was being performed following a

period of preventive

and corrective maintenance.

All personnel

involved with performing the test or post maintenance

testing attended

the brief.

The prejob brief was considered

instrumental

in good coordination of the various post maintenance

tests

performed during the surveillance.

During the time-to-rated-flow and pressure

portion of the test.

the unit

operator

stopped the procedure

and questioned

why the procedure did not

require opening the minimum flow valve prior to starting

RCIC turbine.

After discussions

with the other operators

and system engineer in the

control

room, the operators

determined that this was acceptable

since

the test

was simulating

an automatic initiation and would not be run at

a low flowrate for any significant amount of time.

During the

performance of the surveillance,

control of the operator trainee

performing the test

was good.

Conclusion

The prejob brief for the

RCIC System

Rated

Flow at Normal Operating

Pressure test

was detailed

and instrumental

in successfully coordinating

the performance of the various post maintenance

tests

performed during

the surveillance.

The operator

performing the time-to-rated-flow

portion of the test demonstrated

a good questioning attitude in

questioning the acceptability of an abnormal

system valve lineup.

Control

and supervision of the unit operator trainee

was goo M1.3

Packin

Ad ustment

on Hi h Pressure

Coolant In ection

S stem Steam

Admission Valve

Ins ection

Sco

e

62707

The inspector

reviewed the licensee's

actions

when

a maintenance

worker

adjusted the packing on High Pressure

Coolant Injection (HPCI) system

steam admission valve without work order authorization or operations

approval.

Observations

and Findin s

On June

12,

1998,

a steam leak was found on the Unit 2 HPCI system in

the vicinity of the 2-FCV-73-16 (steam admission valve) packing gland.

This is

a large motor operated

valve that is within the scope of NRC Generic Letter 89-10 and subject to special testing requirements.

Later that day. the steam leak was discussed

at the operations shift

turnover meeting.

Since water was found to be dripping on

a nearby

junction box, the work to be performed

was classified

as Priority 2

This means that work would be performed continuously until completed.

A

maintenance

worker who attended

the meeting discussed

the steam leak

with maintenance

supervision.

The maintenance

worker was then directed

to perform an inspection of the 2-FCV-73-16 steam leak, redirect water

leakage to a catch device,

and to perform inspections of the nearby

electrical junction box.

While inspecting the steam leak, the worker noticed that the packing

gland nuts were loose.

The maintenance

worker tightened the packing

using

a wrench.

However

. the type of packing used

on this valve

requires special

torquing requirements

and

may necessitate

special

valve

testing.

Discussions with maintenance

supervision indicated that the

maintenance

worker believed that adjusting the packing was acceptable

since the work was designated Priority 2 (i.e., urgent)

and had been

discussed

at the operations

turnover

meeting.

A work order was written to check the torque

on the packing gland nuts.

The torque on the packing gland nuts was found to be within

specifications.

Although not required

due to the as found torque, the

licensee successfully

performed motor operated

valve testing to ensure

that the packing adjustment

had not affected the acceptance criteria.

I'he

licensee

conducted briefings with mechanical

maintenance

to discuss

the occurrence

and reiterate the requirements

prior to performing

maintenance

work.

The licensee

also revised

SSP 6.2, Maintenance

Management

System. to require

a control

room pre-job brief before any

maintenance

work is performed

on urgent jobs.

The inspectors

reviewed

SSP-6. 1. Conduct of Maintenance.

and found that the actual

work

performed required approval of operating personnel

prior to work

performance.

This non-repetitive,

licensee-identified

and corrected

violation is being treated

as

a Non-Cited Violation (NCV). consistent

with Section VII.B.1 of the

NRC Enforcement Policy.

This

NCV is

identified as 260/98-04-03.

Unauthorized

Work Performed

on Leaking HPCI

Valve Packing.

Conclusion

A maintenance

worker performed unauthorized

work by adjusting valve

packing without operations

authorization.

Licensee corrective actions

were considered

good.

Additional motor operated

valve testing

was

performed although not required

by the as-tound condition.

Maintenance

and Material Condition of Facilities and Equipment

Unit 3 Torus

0 namic Restraint

Ins ection Sco

e

61726

37551

The inspector

reviewed the licensee's

actions for a leaking torus

dynamic restraint

(snubber)

on Unit 3.

Additionally, the inspector

observed the performance of functional testing of the torus dynamic

restraint following maintenance.

Observations

and Findin s

For several

weeks prior to June 3,

a large Bergen-Paterson

torus dynamic

restraint

(RG-11) located

between the Unit 3 suppression

chamber (torus)

and the reactor building had been leaking oil from the external fluid

reservoir.

The licensee

had been monitoring the oil level

and

periodically added oil as necessary.

Preparations

to replace the

external fluid reservoir with parts

from a Unit

1 torus dynamic

restraint

were initiated.

The inspector

reviewed the basis for snubber operability with a leaking

external fluid reservoir.

A previously completed engineering

analysis

was provided which indicated that an oil addition frequency greater

than

3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> supported

operqbi lity.

The leakage rate basis

ensured

no air

would infiltrate the snubber

main body during

a design basis

loss of

coolant accident.

The inspector

concluded that the evaluation

adequately

supported

snubber operability.

On June 3,

1998. operations

declared the snubber

inoperable

based

on

visual level

and snubber

temperature,

although the level'had not dropped

to the point where air could have been introduced to the main body of

the snubber.

and entered

a 72-hour

LCO in accordance

with TS 3.6.H.

On

the morning of June 4. attempts

were made to refill the snubber

reservoir to an acceptable

level.

While adding oil to the snubber,

the

leakage

increased significantly.

The licensee conservatively

made the

decision to replace the oil reservoi r.

The inspector observed portions of the snubber

reservoir replacement.

No problems were noted.

The licensee

then proceeded to perform

a

functional test

on the snubber

per

3-SI-4.6.H-2C.

Functional Testing of

Bergen-Paterson

Torus Dynamic Restraints.

The functional test strokes

the snubber

and ensures

that no air is in the main body of the snubber.

Additionally, the inspector

observed the surveillance

performance.

Actual testing

was performed using contractors

and contractor supplied

special test equipment.

The inspector observed

good control of the

contractors

throughout the test.

Conclusion

The licensee effectively performed'orrective

maintenance

on

a Unit 3

torus dynamic restraint that had

a leaking oil. reservoi r.

The licensee

maintained

good control of contractor personnel

performing the

functional test of the torus dynamic restraint.

Miscellaneous

Haintenance

Issues

(62707,

92902)

Closed

Violation 260 296/97-05-02,

Failures to Implement Maintenance

Procedures.

The inspector verified the corrective actions

described in

the licensee's

response letter.

dated July 1,

1997, to be reasonable

and

complete.

The Systematic

Assessment

of Licensee

Performance

(SALP)

letter,

dated

May 21 '998,

noted that overall

human performance

compared to the previous

assessment

period improved;

however,

operational

challenges

continued to be caused

by inattention-to-detail

by maintenance

workers.

This was primarily due to problems

encountered

during the earlier portion of the assessment

period (September

8,

1996

through April 18, 1998).

Additionally. the licensee

has taken steps to

systematically track and analyze

human errors in the maintenance

area

as

part of self assessment.

This violation is closed.

Closed

Violation 260 296/97-07-02,

Foreign Material Exclusion Controls

not Implemented in Accordance with Procedures.

The inspector

verified

the corrective actions described

in the licensee's

response

letters,

dated August 14.

1997.

and September

26,

1997, to be reasonable

and

complete.

Recently.

the Browns Ferry site procedure

for foreign

material exclusion

(FHE) controls

was replaced with TVA Nuclear Standard

Programs

and Processes

(SPP) 6.5

~ Foreign Material Control.

The new

procedure simplifies the administration of foreign material exclusion

controls.

For example.

the original site specific procedure established

5 levels of FHE controls whereas

SPP-6.5

has consolidated

and simplified

these

requirements

into 3 levels of controls.

The inspector verified

that the licensee's

corrective procedural

changes

for the violation were

contained in SPP-6.5.

This violation is closed.

Closed

Violation 260/97-09-01,

Functional Testing of Snubbers

While

not in Refueling Outage Conditions.

The licensee

performed

a review to

verify that all other refueling outage

TS surveillances

were

incorporated into the outage surveillance

schedule.

As

a result the

licensee identified an additional

TS refueling surveillance that was not

included in the outage surveillance

schedule.

The inspector verified

that the licensee's

corrective actions

were adequate

and complete.

This

violation is closed.

III. En ineerin

Conduct of Engineer ing

0 eratin

Limit Minimum Critical Power Ratio Correction Coefficient

h

Ins ection Sco

e

37551

The inspector

reviewed the licensee's

actions following the discovery of

an incorrect correction factor to the operating limit minimum critical

power ratio

(OLMCPR).

This correction factor

(TAU) is used to adjust

the

OLMCPR based

on slow control rod scram times.

Observations

and Findin s

On Nay 18,

1998, while performing

a review due to implementing

Improved

Standard

Technical Specifications,

General Electric informed the

licensee that the method

used to calculate the slow control rod

correction factor

(TAU) was incorrect in the Units 2 and

3 Core

Operating Limits Report

(COLR).

Based

on the results of scram insertion

time testing,

TAU is calculated

and adjusts the

OLMCPR.

The

OLMCPR was

determined to be slightly nonconservative

for Unit 3 based

on control

rod scram time testing.

The licensee

placed additional controls

on Unit

3 thermal limits to ensure that the

OLMCPR was not

exceeded.'rior

to Unit 2 cycle 7, the licensee

performed their

own core reload

analysis.

In the 1986 time frame,

General Electric changed the method

used for performing the core reload analysis to an updated version,

Gemini.

The assumptions

used for performing the reload analysis

and in

calculating

TAU were changed to reflect

a newer control rod scram time

statistical

database.

At that time, all three

Browns Ferry units were

in long term shutdown.

The licensee did not update the methodology for

performing the reload analysis

and determining

TAU to reflect changes

in

the database.

The methods

used

by the licensee for calculating

TAU and

the reload analysis

were based

on an older control rod scram time

statistical

databas Beginning with the Unit 2 cycle

7 in 1992,

General Electric has

been

performing core reload analysis for the licensee.

Since the Gemini

method for performing the reload analysis utilizes assumptions

made in

the newer control

rod scram time statistical

database.

the results of

the reload analyses

were not consistent with the licensee's

method for

calculating

TAU.

Consequently.

the

OLMCPR used since then have

been

potentially nonconservative

due to not utilizing the updated control rod

scram time statistical

database

for calculating

TAU.

The licensee

reviewed operating data for the affected cores

(Unit 2

cycles 7.8.9,

and

10 and Unit 3 cycles

7 and 8).

The data also showed

that the

OLMCPR was not exceeded

at any time while the incorrect method

of calculating

TAU was employed.

Therefore,

no potential for exceeding

the Safety Limit MCPR (if an abnormal

operating transient occurred)

existed during the affected operating cycles.

The inspector

reviewed

the licensee's

methods for determining whether the

OLMCPR was exceeded.

The inspector

found that conservative

methods

were used (e.g.,

using the

worst

TAU for any fuel bundle type with the wor'st case

MCPR value).

The

licensee also reviewed the methods for calculating the other thermal

limits and found that they were not dependent

on the different database

methods (i.e.,

Genesis

or Gemini).

The inspector

reviewed the licensee's

corrective actions (i.e., placing

additional restrictions

on OLMCPR, revising the

COLRs, making necessary

software changes to the Integrated

Computer System

and 3D-Monicore) and

determined that they were performed promptly.

The licensee attributed

the root cause of using the incorrect values of TAU to the process that

changed the responsibility for performance of the reload analysis to a

different organization.

As a result of review of the Institute of Nuclear Power Operations

(INPO) Significant Operating Experience

Report 96-2.

Design

and

Operating Considerations

for Reactor

Cores,

the licensee

has instituted

upgrades to the review process for core reload analyses

(SPP 10.8,

"Nuclear

Fuel

Management,

Rev. 1").

These include increased

coordination

and communication

between

design organizations,

additional

reviews at designated

stages

throughout the core reload design

process'nd

increased

licensee oversite to the vendor's control of design input

and calculational

methods.

The inadequate

method for control of the design interfaces

and for

coordination

among participating design organizations

constitutes

a

violation of 10 CFR 50, Appendix 8, Criteria III, Design Control.

This

non-repetitive,

licensee-identified

and corrected violation is being

treated

as

a Non-Cited Violation, consistent with Section VII.B.1 of the

NRC Enforcement Policy.

This

NCV is identif'ied as 260.296/98-04-04.

Incorrect

TAU Constant

Used to Adjust Operating Limit MCP Conclusion

E8

E8.1

The correction coefficient

(TAU) 'used to adjust the operating limit HCPR

for slow control rod scram insertion times was incorrect for several

Unit 2 and

3 operating cycles,

however,

the corrected

OLHCPR was never

exceeded.

Weak design controls were in place

between the licensee

and

the contractor performing core reload analysis.

The licensee corrective

actions were prompt and complete.

Hiscellaneous

Engineering

Issues

(92903)

Closed

Unresolved

Item 260 296/97-03-01

~ Review of Switchyard Control

Power.

Following a loss of offsite power to Unit 3 during

a refueling

outage.

the inspectors

had noted that switchyard control

power was

supplied by one battery board

and questioned

whether this met the intent

of General

Design Criteria

(GDC) 17.

A request for Technical Assistance

(TIA 97-008)

was submitted for Nuclear Reactor Regulation

(NRR) review.

On June

12,

1998.

NRR completed review of the issue

and concluded that

the

BFN offsite power system design

meets the requirements of GDC 17.

The Unresolved

Item is closed.

E8.2

Closed

Ins ection Follow-u

Item 260 296/97-007-03,

Spent

Fuel

Pool

Cooling System Heat

Removal Capacity.

During Follow up of inspector

observations

that predicted spent fuel pool temperatures

during

refueling outage activities did not match actual

pool temperatures,

the

inspectors

noted that the licensee's

practice of calculating time after

shutdown at which the fuel pool gates could be installed was not

reflected in the description of Spent

Fuel

Pool Cooling System

(SFPCS)

capacity in the Updated Final Safety Analysis Report

(UFSAR).

Immediately following a core off-load of 1/3 of the core to the pool,

the gates

separating

the pool from the reactor cavity are not installed

since the

SFPCS

does not have capability to remove the decay heat.

The

licensee

performs calculations of the decay heat

and determines

the time

at which the gates

could be installed.

Section 10.5.5 of the

UFSAR

states that the

SFPCS

can keep pool temperatures

below 125 degrees

F

when removing maximum normal heat load from the pool with maximum

reactor building closed cooling water

(RBCCW) temperatures.

It should

be noted that supplemental

spent fuel pool cooling

(RHR system assist)

is normally available to cool the spent fuel pool if necessary.

In response to the inspector's

questions,

the licensee initiated Problem

Evaluation Report

(PER) 971322.

The SFPCS

system engineer

performed

a

detailed review of the issues.

In addition to confirming that the

UFSAR

did not adequately

describe the

BFN practice regarding fuel pool gate

installation and

SFPCS capacity,

the engineer

identified several

other

deficiencies:

Cl

The value listed in UFSAR Table 10.5-1

as

"maximum possible heat

load" was

not correct.

The value of 29E+06 BTU/hr was based

on

16 day minimum core off-load time which is no longer valid.

The

actual

value for maximum heat load is dependent

on calculated

heat

removal

system capability

and administrative controls

on fuel pool

gates.

The licensee

performed

a detailed calculation of current

actual

SFPCS

and

RHR assist

fuel pool cooling capacities.

The

results indicated

a total capacity of 35E+06 BTU/hr at

150 'F

which bounded the 29E+06 BTU/hr value listed in the

UFSAR.

The

inspector

noted that the calculation included allowances for heat

exchanger

tube plugging and used conservative

values of RHR

.service water temperature.

Outage Risk Assessment

and Hanagement

(ORAN) calculations for heat

removal capability of the

SFPCS did not consider that heat

exchanger

tube plugging had reduced the capacity below design

value.

Detailed review indicated that the actual

SFPCS capacity

was less

than the value (27.6E+06

BTU/hr at

125 'F) included in a

1977

submittal to the

NRC for

a high density fuel storage

system

(HDFSS).. The actual

value was about

19E+06 BTU/hr at 125 'F which

corresponds,to

about

35E+06 BTU/hr at 150 'F.

As stated in

section 10.5.5 of the

UFSAR,

125 'F is

a normal operational

limitation on SFP water temperature,

150 'F is

a maximum limit for

larger than normal core off loads,.

If temperature

appears

to be

likely to exceed

125 'F

RHR assisted

fuel pool cooling is

available to maintain temperature

less than

150 'F for the benefit

of personnel

working near the SFP.

The effect of the different

heat values

was not significant since

35E+06 BTU/hr at

150

F

bounded the heat load of Z9E+06 BTU/hr at

150 'F.

While the total

.margin assumed

in the Safety Evaluation Report

(SER) was not

available,

the conclusions

continued to be valid.

As discussed

above.

an error had caused

inaccurate

fuel pool

cooling capacities to be documented.

That information was used in

a 1996 safety assessment

to increase

the maximum possible fuel

pool cooling heat load values in the

UFSAR from 27.6E+06 BTU/hr to

29E+06 BTU/hr.

Additionally, the licensee

noted that

a safety

evaluation

was not completed since the

UFSAR change

was considered

insignificant because it reflected values in the 1977

HDFSS

submittal

and

SER.

The change

was based

on

a 1978

NRC (SER) in

which the

NRC interpreted the TVA full decay heat load curve as

Z9E+06 BTU/hr after

16 days.

As discussed

above.

the actual

heat

removal capacity

(35E+06BTU/hr at

150 'F) was well above the decay

heat load In March 1998,

UFSAR Change

Package

17-001

was completed.

The change

revised. the values listed in Table 10.5-1 to reflect design capacity

heat

removal capabilities.

The change also clarified how BFN assures

that heat loading is withi'n capabilities of the SFPCS.

RHR assist,

and

Additional Decay heat

Removal

(ADHR) systems.

ADHR is

a recently

installed large capacity cooling system designed to cool the fuel pool

and connected

volumes during refueling outages.

The revision is

expected to be incorporated into UFSAR revision 17.

The licensee

attributed the cause of the

UFSAR not reflecting the actual

operation to

inadequate

documentation of changes.

The licensee is still in the process of a detailed

programmatic

examination of the

UFSAR.

Revision

2 of Technical Instruction (TI)-353

contains

guidance

on the current review process.

The licensee is

utilizing a team review approach with different site groups

represented

on the team.

The review has

been identifying on differences

between

UFSAR descriptions

and actual

operations

such

as this issue.

ORAM methodology

has

been revised to ensure that updated

SFPCS

heat

exchanger

data is used for calculations of decay heat

removal

capacities.

Recent predicted fuel pool temperatures

have been very

close to actual

values.

The actual capacity of the

RHR assist

mode of

fuel pool cooling was calculated

as described

above.

Licensing reviewed

the results

and determined that no issues

existed which required

reporting to the

NRC.

TVA has significantly strengthened

50.59 procedures

since the 1996

safety assessment

was completed.

A safety evaluation is required for

any

UFSAR changes.

The inspectors

concluded that the licensee's

engineer

performed

a

thorough review of the issues.

While NRC inspectors

had identified that

the

UFSAR description of fuel pool heat loading did not reflect actual

operating practices,

the licensee's

review identified several

other

deficiencies.

The inspectors

have observed that refueling outage

activities are well scheduled

and. DRAM is emphasized

during the outages.

Corrective actions were completed,

including detailed calculations of

fuel pool cooling capabilities

and revision of the

UFSAR, within an

acceptable

time period.

Although the

UFSAR did not accurately reflect

the actual

operating practices

regarding the spent fuel pool gates,

the

potential safety role of the

SFPCS is limited.

In safety analyses.

emergency

fuel pool

makeup is relied upon to maintain the pool inventory

sufficiently high to prevent spent fuel damage.

There have

been

no

problems associated

with fuel pool cooling capacity

BFN, pool

temperatures

have

been maintained within operating limits.

This

inspection follow-up item is close E8.3

Closed

Ins ection Follow-u

Item 296/98-01-03,

Slow Control

Rod Arrays

Five Percent

Insertion Scram Times.

This item addressed

slow five

percent insertion times for four groups of control rods attributed

to

sticking exhaust

valve scram solenoid pilot valves

(SSPVs).

The

inspection follow-up item was opened

because

the cause of the problem

had not yet been determined.

The licensee

had requested

evaluation

of=

the slow SSPVs

by General Electric and Automatic Switch Company

(ASCO).

The inspector

reviewed the evaluation which concluded that

a root cause

could not be determined.

Testing

was performed

by mounting the valve

internals inside new SSPVs.

aging the assemblies

and testing for delays.

Although the testing confirmed that

some sticking occurs with the Buna-N

material.

ASCO was not able to duplicate the increased

response

times

seen

by the licensee.

No evidence

was found of contamination in the

control air system or lubricant effecting the elastomer material.

The inspector

reviewed the corrective actions listed in Problem

Evaluation Report 98-0089

and concluded that the licensee's

actions to

date

have been

adequate to address

the problem.

Insertion times since

the January

1998 incident have

been within requirements

and no other

pattern of degradation

has

been identified.

In response to questioning.

the licensee

indicated that plans are to replace the Buna-N material

with an upgraded

Viton material in about

50 percent of the hydraulic

control units during the next refueling outage

(September

1998).

Engineering indicated that the material would be within service life

limits through the next operating cycle.

The inspector

requested

verification that the Buna-N material

was not restricted

by the total

accumulated

"shelf life" and service life.

A licensee

engineer

subsequently

identified that Environmental Qualification binder

BFNEQ-

SOL-004 contains

a statement that the material

was to be replaced after

ten years

from date of manufacture or five years of service life,

whichever occurs first.

Other information in the

BFN harsh

environmental

data

base simply stated that the Buna-N material is to

replaced after five years of service life.

The Buna-N material in the

Unit 3 exhaust

diaphragms is at or greater

than ten years

from date of

manufacture.

PER 98-007412-000

was initiated to address this issue.

General Electric Service Information Letter (SIL) 585, dated January

4,

1995,

addressed

SSPV and air system maintenance.

The inspectors

reviewed the SIL and noted that the SIL specifically states

that service

time guidelines

assume that service time occurs after

maximum

recommended

storage

time.

The SIL lists eight years

as

recommended

maximum storage

time and 4 years

maximum energized application service

life.

The SIL stated the storage conditions that are assumed for

storage time limitations.

The inspectors verified that the actual

storage conditions for the spare

diaphragms

matched those described

in

the SI The licensee

indicated that although the cure date for the Buna-N

diaphragms installed in Unit 3 was not available. it was reasonable

to

conclude that the diaphragms installed in Unit 3 in February

1996 are

generally in compliance with the SIL recommendations.

The inspector

reviewed purchase

documentation

which described

a large quantity of

solenoid valve parts kits that were received in October

1988.

Shelf

life documentation

indicated

a ten year life span.

The

SSPVs were

placed in service

on Unit 3 in February

1996, which is within eight

years of the receipt date.

The licensee

does not expect

any material

degradation

problems throughout the remaining planned service period.

This item is closed.

IV. Plant

Su

art

Radiological Protection

and Chemistry

(RP8C) Controls

Ins ection Sco

e

83750

84750

The inspectors

reviewed implementation of selected

elements of the

licensee's

radiation protection program.

The review included

observation of radiological protection activities including personnel

monitoring, radiological postings,

high radiation area controls,

and

verification of posted radiation dose rates,

contamination controls

within the radiologically controlled area

(RCA), and container labeling.

In addition, observations

were made of ALARA work planning, pre-job

worker briefings,

and job execution.

The inspectors

also reviewed

licensee

records of personnel

radiation exposure

and discussed

ALARA

program details,

implementation

and goals.

Requirements

for these

areas

were specified in 10 CFR 20 and TSs.

Observations

and Findin s

The inspectors

toured the health physics facilities, the Reactor

and

Turbine building and outside radioactive material storage

areas

(RNSAs).

From review of records,

the inspectors

determined

the licensee

was

tracking and trending personnel

contamination

events

(PCEs).

The

licensee

had tracked approximately

PCEs for the 1998 fiscal year to

date which included skin and clothing contaminations.

This equates

to

approximately 3.3

PCEs

per

1000

RWP hours.

Radiologically controlled

areas

including RNSAs, High Rad Areas,

and Locked High Rad Areas were

appropriately posted

and radioactive material

was appropriately stored

and labeled.

Selected

boundaries

were independently

measured

by the

inspectors

and the dose rates

measured

were comparable to the posted

rates.

The inspectors

reviewed operational

and administrative controls for

entering the

RCA and performing work.

These controls included the use

of radiation work permits

(RWPs) that were to be reviewed

and understood

by workers prior to entering the

RCA.

The inspectors

reviewed selected

'WPs

and observed

RWP briefings for adequacy of the radiation protection

requirements

based

on work scope.

locations

and conditions.

For the

RWPs reviewed.

the inspectors

noted that appropriate protective

clothing.

and dosimetry were required.

During tours of the plant, the

inspectors

observed the adherence

of plant workers to the

RWP

requirements.

The inspectors

observed

workers properly entering the

controlled area

by signing on to the Radiation

Exposure

System

(REXS).

The inspectors

observed that personal

dosimetry was being worn in the

appropriate location.

The inspectors

observed

workers properly using friskers at the exit

locations

from controlled areas.

The inspectors

also observed

workers

properly exiting the protected

area through the exit portal monitors

located at the East

and West security portals;

The Fiscal

Year 1998 site exposure

goal

was set at 450 person-rem.

At

the time of the inspections

the site person-rem

was about 390.67 person-

rem TLD corrected through March 31,

1998.

The inspectors

reviewed the Contaminated

Square

Footage

Data for FY 98.

At the time of the inspection there were approximately

1070 contaminated

square feet(ft').

This includes approximately 130ft'rom

UO (common),

355ft'rom Ul, 370ft'rom U2,

and 215ft'rom U3.

This was slightly

more than the goal of 1000ft'.

The licensee tracks the contaminated

.

area

as

a running 30-day average

and at the time of the inspection the

previous 30-day average

was 1140ft'.

Decontamination,

scheduled for

approximately 120ft'n the reactor building of Unit 2 on June

29.

1998.

would reduce the contaminated

area to approximately 950ft'hich would

be below the 1000ft'oal.

The inspectors

attended

a meeting

and reviewed minutes of three previous

meetings of the High Impact Team (HIT) assigned

the Unit 3 Drywell

Decontamination.

The team is Chaired

by the Radwaste/Environmental

Supervisor

and consists of members

from Site Engineering,

Radcon,

Maintenance,

In-Service Inspections

Operations

Outage.

and Outage

Scheduling.

The multi-discipline team was constituted to determine the

best course of action on how to decontaminate

the

U3 Drywell which had

become contaminated

in the vicinity of an instrument sensor line leak.

Several of the smear

results

showed transferrable

contamination in

excess of 2E+6 dpm/100cm'.

Equipment lists by elevation,

location and

equipment protection requirements

had already

been factored in the plan.

The licensee

was evaluating the dress out and heat stress

factors,

had

polled the industry for like experiences

and was aggressively

planning

for the

U3 drywell decontamination

campaign.

The inspectors selectively reviewed the whole body counting program

procedures.

RCI-8 titled Bioassay

Program Revision 13, dated 02/03/98,

RCI 8.1 Internal Dosimetry Program

Implementation Revision 22A. dated

01/05/98,

the January

12,

1998 Whole Body Counting Measurement

Quality

Assurance

Report and the daily calibration checks.

The inspectors

determined that the licensee

was following the requirements of the

reviewed procedures.

The Quality Assurance

checks

were performed

as

requi red and the daily 'calibration checks

were also performed

as

required.

The tracking and trending of count data were performed

as

required

and the system

met Minimum Detectable Activity values.

Conclusion

Radiological facility conditions in radioactive waste storage

areas,

health physics facilities and Turbine and Reactor Buildings were found

appropriate

and the areas

we'e properly posted

and material

appropriately labeled.

Personnel

dosimetry devices

were appropriately

worn.

Radiation work activities were appropriately planned.

Radiation

worker doses

were being maintained well below regulatory limits and.the

licensee

was maintaining exposures

ALARA.

A special

team was

aggressively

planning the

U3 drywell cleanup.

The Whole Body counting

program was performed

as procedurally required.

V. Mana ement Meetin s

X1

Exit Meeting Summary

The resident inspectors

presented

inspection findings and results to

licensee

management

on July 15,

1998.

An additional

formal meeting to

discuss

inspection findings was conducted

on June

26,

1998.

X3

Hanagement

Meeting Summary

The Browns Ferry Systematic

Assessment

of Licensee

Performance

was

presented to the licensee at the Browns Ferry site in a public meeting

on July 11,

1998.

PARTIAL LIST OF

PERSONS

CONTACTED

Licensee

T. Abney, Licensing

Manager

J. Brazell, Site Security Manager

R. Coleman,

Acting Radiological

Control

Manager

J.

Corey, Radiological Controls

and Chemistry Manager

C. Crane, Site Vice President.

Browns Ferry

R. Greenman,

Training Manager

J. Johnson'ite

Quality Assurance

Manager

R. Jones,- Assistant Plant

Manager

R. Moll, System Engineering

Manager

G. Little. Operations

Manager

D. Nye, Site Engineering

Manager

D. Olive. Operations

Superintendent.

J.

Shaw,

Design Engineering

Manager

K. Singer,

Plant Hanager

J. Schlessel.

Maintenance

Manager

IP 37551:

IP 62707:

IP 61726

IP 71707:

IP 71750:

IP 93750:

IP 84750:

IP 92901:

IP 92902:

IP 92903:

INSPECTION

PROCEDURES

USED

Onsite Engineering

Maintenance

Observations

Surveillance

Observations

Plant Operations

Plant Support Activities

Occupational

Radiation

Exposure

Radioactive

Waste Treatment,

and Effluent and Environmental

Monitoring

Follow-up-Plant Operations

Follow-up-Maintenance

Follow-up-Engineering

ITEMS OPENED AND CLOSED

OPENED

T~e

Item Number

Status

Descri tion and Reference

NCV

296/98-04-01

IFI

260.296/98-04-02

NCV

260/98-04-03

NCV

260,296/98-04-04

Closed

Open

Closed

Closed

Failure to Follow Procedure

for

RHR

Fill and Vent (Section 01.2).

Use of Maintenance

and Test

Equipment (Section Hl.1).

Unauthorized

Work Performed

on

Leaking

HPCI Valve Packing (Section

M1.3).

Incorrect

TAU Constant

Used to

Adjust Operating Limit HCPR (Section

E1.1).

CLOSED

T~e

Item Number

Status

Descri tion and Reference

VIO

296/97-05-01

URI

260/97-010-02

Closed

Closed

Failure to Reset

Locked Scoop Tube

(Section 08.1).

Technical

Speci ficati on Requirements

During Control

Rod Drive (CRD)

LER 296/97-004-00

VIO

296/97-10-03

VIO

260,296/97-05-02

VIO

260.296/97-07-02

VIO

260/97-09-01

URI

260.296/97-03-01

IFI

260.296/97-007-03

IFI

296/98-01-03

Closed

Closed

Closed

Closed

Closed

Closed

Closed

Closed

Accumulator Maintenance

(Section

08.2).

Unplanned

Hanual Start of an

Emergency

Diesel Generator

During

a

Scheduled

Redundant Start Test

(Section 08.3).

Failure to Complete

TS Action for

Inoperable

Containment

Isolation

Valve (Section 08.4).

Failures to Implement Maintenance

Procedures

(Section

H8. 1).

Foreign Material Exclusion Controls

not Implemented in Accordance with

Procedures

(Section H8.2).

Functional Testing of Snubbers

While

Not in Refueling Outage Conditions

(Section H8.3).

Review of Switchyard Control

Power

(section E8.1).

Spent

Fuel

Pool Cooling System Heat

Removal

Capacity (Section E8.2).

Slow Control

Rod Arrays Five Percent

Insertion

Scram Times (Section

E8.3).

Ip