ML18038B979

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Insp Repts 50-259/97-09 50-260/97-09 & 50-296/97-09 on 970803-0913.Violations Noted.Major Areas Inspected: Licensee Operations,Engineering,Maint & Plant Support
ML18038B979
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 10/08/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18038B977 List:
References
50-259-97-09, 50-259-97-9, 50-260-97-09, 50-260-97-9, 50-296-97-09, 50-296-97-9, NUDOCS 9710230009
Download: ML18038B979 (62)


See also: IR 05000259/1997009

Text

U.S.

NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

License

Nos:

50-259.

50-260.

50-296

DPR-33.

DPR-52.

DPR.-68

Report

Nos:

50-259/97-09,

50-260/97-09.

50-296/97-09

Licensee:

Tennessee

Valley Authority

Facility:

Browns Ferry Nuclear Plant.

Units 1, 2,

8 3

Location:

Corner of Shaw and Browns Ferry Roads

Athens'L

35611

Dates:

August

3 - September

13,

1997

Inspectors:

Approved by:

L. Wert, Senior Resident

Inspector

(SRI)

J. Starefos,

Resident

Inspector

D. Thompson,

Special

Inspections

Inspector

(Sections

S3

~ S6,

S7

~

SB)

P.'aylor,

Project Engineer

C. Patterson,

SRI

- Brunswick

(Sections

08. 1,

MB. 1-8.3, E8.2-8.3)

M. Lesser,

Chief

Reactor Projects

Branch

6

Division of Reactor Projects

Enclosure

2

9710230009

971008

PDR

ADQCK 05000259

G

PDR

0

0

EXECUTIVE SUMMARY

Browns Ferry Nuclear Plant.

Units l. 2,

8 3

NRC Inspection

Report 50-259/97-09,

50-260/97-09,

50-296/97-09

This integrated

inspection included aspects

of licensee operations,

engineering,

maintenance,

and plant support.

The report covers

a six-week

period of resident

inspection

and inspection in the security area

by a

Region II inspector.

0 erations

Initial review of the failure of containment isolation valve 3-FCV-64-34 to

close during

a test raised questions

regarding the operability status of the

valve when it failed to close after the problem was believed to have been

resolved.

Additional review of the sequence

of events

and the specific

failure mechanism is necessary

to determine if a violation of regulatory

requirements

occurred.

(Unresolved

Item 50-296/97-09-06,

Actions for

Inoperable

Containment Isolation Valve, Section 01.1).

During Plant Operations

Review Committee

(PORC) meetings,

the committee

conducted

good reviews of the presented

material.

PORC members

asked probing

uestions

regarding the overall safety of the activities and appropriately

ocused

on whether

the change

represented

an unreviewed safety question or was

prohibited by Technical Specifications.

(Section 07. 1)

Maintenance

The inspectors identified that the licensee

was not properly implementing

procedural

controls over scaffolding in the Unit 2 reactor building.

In some

cases,

scaffolds near safety related

equipment

were not constructed

in

accordance

with limitations in the procedure

or in the requi red engineering

evaluation.

The scaffolding assembly checklist was not being properly

completed.

Some procedural

requirements,

which would be difficult to

complete,

were not being implemented.

No safety systems

were rendered

inoperable

by the noted deficiencies.

The inspectors

concluded that the

number

and nature of the deficiencies indicate that supervisory personnel

are

not enforcing standards

and failed to ensure that procedural

requi rements

are

satisfactorily met. (Violation 260/97-09-02,

Scaffolding Controls Not Properly

Implemented,

Section M1.1).

The inspectors

identified that the licensee

was conducting functional testing

of snubbers

on safety related

systems with the unit at power.

Technical

specifications state that snubber

functional testing is to be performed during

refueling outages.

Procedural

controls for the testing did not adequately

enforce the

TS requirements.

(Violation 260/97-09-01.

Functional Testing of

Snubbers

While Not in Refueling Outage Conditions.

Section M1.2).

~

Cl

41

Observation of several

selected

maintenance activities indicated that the work

was well planned

and executed.

Specifically,

As Low As Reasonably

Achievable

(ALARA) planning of contingencies

was good with regard to the high radiation

evolution observed.

The prejob brief in preparation for C3 emergency

equipment cooling water

pump work was strong.

(Sections Hl.3-1.5)

En ineerin

Review of residual

heat

removal

system service water

pump inservice testing

data

and methodology indicated that the repeatabi lity and effectiveness

of the

testing could be improved.

Inspection

Followup Item 50-260,296/97-09-07,

RHRSW/EECW

Pump Flow Testing Issues.

(Section El. 1)

The licensee's

actions

regarding pressurization

of portions of the Unit 2

shutdown cooling suction piping were acceptable.

The licensee

pursued the

problem in a reasonable

manner

and the present

conditions

do not represent

an

immediate safety concern.

Licensee

management

has indicated that the intent

is to effectively address

the issue

such that it will not exist once the unit

is returned to power after the refueling outage.

(Section

E2. 1)

Plant

Su

ort

A random review of plans,

records.

reports,

and interviews with appropriate

individuals verified that security plan and procedure

changes

did not decrease

the effectiveness

of the Physical Security Plan.

(Section

S3. 1)

Licensee

management

provided appropriate

and excellent support for the

Physical Security Program.

Examples of the excellent

management

support were

the support in preparation for the Operational

Safeguards

Response

Evaluation

and the excellent maintenance

and engineering

support for the security

equipment.

(Section

S6. 1)

The lic'ensee

evaluated

hardware

and mechanical

problems associated

with

security equipment

and the problems were effectively controlled and managed.

(Section S6.2)

Licensee-conducted

audits were thorough.

complete.

and effective in terms of

uncovering weaknesses

in the security system,

procedures,

and practices.

The

last audit report concluded that the security program was effective and

recommended

appropriate action to improve the effectiveness

of the security

program.

The licensee

had acted appropriately in response

to recommendations

made in the audit report.

(Section S7.1)

High pressure fire protection system flushing was completed according to the

work instructions.

The procedure

was actively utilized and the workers were

knowledgeable of the evolution.

Radio communications

were appropriately

formal and the workers were careful

when draining the system to minimize

overflow of the floor drains.

(Section

F2)

II

Summar

of Plant Status

Re ort Details

Unit 1 remained in a long-term lay-up condition with the reactor defueled.

Unit 2 reduced

power to 83K on August 18,

1997,

due to a water leak in the 2A

high pressure

heater

room.

On August 23,

1997, the

U2C9 coastdown

began with

all rods out, recirculation flow at 100K.

and final feedwater reduction

implemented.

Unit 3 operated

at or near full power with the exception of routine testing

and scheduled

maintenance

downpowers.

During some of the inspections

discussed

in this report, the inspectors

reviewed applicable portions of'he Updated Final Safety Analysis Report

(UFSAR) that related to the areas

inspected.

No deficiencies

were identified

during the reviews.

01

Conduct of Operations

I. 0 er ations

01. 1

Su

ression

Chamber

Standb

Gas

Inboard Isolation Valve

~571707

The inspectors

reviewed licensee actions taken after the suppression

chamber standby

gas inboard isolation valve (3-FCV-64-34) failed to

close during

a surveillance test

on July 26,

1997.

b.

Observations

and Findin s

On July 26.

1997, during surveillance testing.

the licensee identified

that valve 3-FCV-64-34 failed to close when demanded.

This valve is

a

Group 6 containment isolation valve located in piping connected to the

suppression

chamber.

The valve closed during

a subsequent

attempt

and

was cycled several

additional times.

The licensee

began cycling the

valve once every. four hours to ensure continued operability.

The

licensee

submitted

a work request to repair the valve and subsequently

issued

a Technical Operability Evaluation

(TOE) on July 29,

1997.

The

TOE analysis

determined that continued operation,

every four hours. of

the valve was

no longer necessary

and that

CR120 relay 86-64-34 would be

replaced.

In the past,

the

CR120 relays

had been observed to stick in

the energized position if they were energized for a long period of time.

The licensee

concluded that the primary containment isolation system

(PCIS) closure function of the 3-FCV-64-34 valve would not be inhibited

by the problem with the 86-64-34 relay.

TOE 3-97-064-1159,

Revision

0

concluded that valve 3-FCV-64-34 would perform its safety function and

that the system

remained operable.

0

Cl

4l

J

On August 14,

1997 'he 3-FCV-64-34 valve failed to close again

when

tested.

The 86-64-34 relay was replaced

on August 19,

1997,

and post

maintenance testing

was completed satisfactorily.

On August 24.

1997,

the 3-FCV-64-34 valve failed to close during performance of surveillance

testing.

The valve handswitch

was cycled two more times before the

valve closed.

The licensee

determined that the

TOE still applied. there

was not

a PCIS operability concern,

and continued troubleshooting.

On

August 28.

1997, with a contingency work order

planned for immediate

replacement of the solenoid valve associated

with 3-FCV-64-34, another

attempt

was

made to close the 3-FCV-64-34 valve.

The valve took several

seconds to close following operator

action to turn the handswitch to the

close position.

The licensee

declared the valve inoperable

due to slow

closure time and subsequently

replaced the

ASCO solenoid valve which is

used to control the 3-FCV-64-34 valve.

(Section N1.5 of this report

describes

NRC inspection of the replacement activity.)

A failure of the

solenoid valve would affect the ability of the valve to close which is

the

PCIS required position.

After reviewing the sequence

of events

associated

with the valve

failure, the inspectors

questioned

licensee

management

regarding the

valve operability status

on August 24 when it failed to close after the

problem was believed to have been resolved.

Licensee

management

reviewed the event

and concluded that

TS requirements

for

an inoperable

containment isolation valve had not been

met.

The licensee

plans to

submit

a 10CFR50.73 report.

This issue is identified as Unresolved

Item (URI) 50-296/97-09-06,

Actions for Inoperable

Containment Isolation Valve, pending additional

review of details regarding the timeliness of the licensee's

actions.

The licensee is reviewing the cause of the solenoid valve failure.

Preliminary indications are that sticking at the core-plugnut interface

(CPI) may have contributed to the failure.

The licensee

disassembled

the solenoid valve and identified that

a varnish-like substance

existed

at the CPI.

The licensee

plans to remove two additional solenoid valves

used in similar applications in the plant, in addition to the failed

solenoid valve.

and have

an evaluation performed.

A similar problem

was previously identified in Inspection

Followup Item

( IFI) 260.296/95-

64-10,

Secondary

Containment Ventilation

Damper

Failures,

and updated in

NRC Inspection

Report 259,260,296/96-008.

IFI 260,296/95-64-10

remains

open.

c.

Conclusions

The inspectors

concluded that since the licensee

had initially

identified the

CR120 relay as the apparent

cause of the symptoms

and had

replaced the relay, the 3-FCV-64-34 valve should have been declared

inoperable

when it subsequently

failed. Additional review of the

sequence of events is necessary

to determine if a regulatory violation

occurred.

0

0

01.2

Observation of Assistant Unit 0 erator

Rounds

a.

Sco

e

71707

The inspectors

observed

the Unit 3 Rounds Assistant Unit Operator

(AUO)

while he performed portions of Turbine Building Rounds.

b.

Observations

and Findin s

On August 30,

1997, the inspector

observed

the Unit 3 Rounds Assistant

Unit Operator

(AUO) while he performed portions of Turbine Building

Rounds.

The inspector

noted that, in light of recently identified

scaffold problems,

the

AUO was sensitive to scaffolding in the plant.

The inspector also noted that the

AUO initiated work requests

for

identified problems

and mairitained housekeeping.

07

Quality Assurance in Operations

07. 1

Plant

0 erations

Review Committee Meetin

a.

Ins ection Sco

e

71707

The inspectors

attended

four Plant Operations

Review Committee

(PORC)

meetings.

In addition to assessing

the quality of the reviews, the

inspectors verified that selected

requirements of Technical Specification 6.5. 1 and Site Standard

Practice

SSP-12. 10, Plant

Operations

Review Committee,

were met.

b.

Observations

and Findin s

Each of the meetings

was chai red by the Acting Operations

Manager.

It

was clear that he was in charge of the meetings.

An appropriate

level

of formality was maintained during the meetings.

The committee actively

questioned

individuals presenting

material for review.

The

PORC

composition

met the requi rements of TS 6.5. 1.2.a.

Specific items noted:

~

During review of a safety evaluation for use of a temporary

power

supply for the neutron monitoring system during

a battery

replacement,

the

PORC asked detailed questions

regarding the

qualification of the temporary supply.

The evaluation

was not

approved since the presenter

could not answer

several of the

PORC's questions.

e

The

PORC did not approve

a request to delete

Updated Final Safety

Analysis Report

(UFSAR) section

13. 10.2.8 which described

feedwater

system operational testing.

The

PORC indicated that the

UFSAR description should

be revised to reflect the proper testing

criteria if the current description is inaccurate,

but the section

should not be deleted.

0

08

08.1

08.2

~

The

PORC did not approve

a proposed

design

change associated

with

the main steam relief valve automatic actuation logic since there

were too many items remaining

as

"open" in the proposed

modification.

o

The

PORC chairman

ensured that only authorized

personnel

were

present

when an issue involving safeguards

information was

discussed.

~

The

PORC reviewed

"A" level Problem Evaluation Report 960204.

UFSAR Issues.

The

PORC requested

that the presenters

return with

stronger explanations of the underlying issues

and corrective

actions.

Conclusions

The inspectors

concluded that the

PORC conducted

adequate

reviews of the

presented

material.

PORC members

asked probing questions

regarding the

overall safety of the activity and focused

on whether the change

represented

an unreviewed safety question or was prohibited by Technical

Specifications.

Miscellaneous

Operations

Issues

(92901)

Closed

Licensee

Event

Re ort

LER 296/96-002-00

Unit 3 Scram

Following Loss Of Reactor

Feedpump

3C.

This event was discussed

in

Inspection

Report 96-04.

The cause of the scram

was due to low reactor

water level caused

by loss of the

3C reactor

feedpump resulting from

improperly aligned oil valves.

A personnel

error occurred while

aligning the feedpump oil tank to the purification system.

The oil tank

was drained causing the feedpump to trip.

The plant design is such that

a loss of a single reactor

feedpump

can

be compensated

for by increased

output of the other

two reactor

feedpumps

in combination with an

automatic

run back of the reactor recirculation

system

pumps.

In this

case reverse flow occurred through the

3C reactor

feedpump line due to

a damaged

discharge

check valve.

The damage to the check valve was also

discussed

in Inspection Report 96-04 with long term resolution of this

problem tracked

by Inspection

Followup Item 296/96-04-04 that remains

open.

Personnel

corrective action was taken with the operator

responsible for the valve misalignment.

The inspector

reviewed the

Inspection

Report

and

LER.

All issues

had been previously discussed

or

tracked.

This

LER is closed.

Closed

Violation 296/96-12-01,

Failure to Ensure Proper Position of

EDG Aux Board

Room Exhaust

Fans.

This violation addressed

instances

in

which

NRC inspectors

found the switches for the Unit 3

EDG auxiliary

board

room exhaust

fans not positioned in accordance

with the system

Operating Instruction.

The inspector verified that procedures

0-OI-30F

and 0-GOI-300-1 have been revised to clearly indicate when the fans can

be turned off.

OI-30F states that the fans shall

be operating

when

ambient outside temperature

is 40 degrees

F or above.

Verification of

the Unit 3 exhaust

fans

has also been

added to procedure

O-GOI-300-1.

. Il

4l

0

08.3

The inspectors

have noted

on tours that the fan control switches

have

been'aintained

in the correct position and that the fans were running.

Currently, caution tags are installed

on the Unit 3 fan switches to

ensure that the fans remain energized.

The violation is closed.

CLOSED

Violation 296/96-13-03,

Uncontrolled Locked High Radiation Area

(LHRA).

This violation occurred

on December'7,

1996, while the Unit 3

3Al/3A2 Heater

Room, which is normally posted

as

a

LHRA, was de-posted

to support maintenance activities when extraction steam

was isolated.

The area 'became

a High Radiation Area again

when operations

personnel

inadvertently introduced

a radiation source to the room by manipulating

an extraction

steam valve.

The inspector verified that the latest revision of Operating Instruction

3-0I-6. Feedwater

Heating

and Misc Drains System,

included

a statement

to notify Radcon personnel

prior to making changes

in Feedwater

Heating

System alignments

which could cause

a rise in area radiation levels.

The procedure further required confirmation, to be obtained prior to

performing the alignment, that Radcon

has

implemented appropriate

radiological controls/barriers

for the expected

Feedwater

Heating System

alignment.

In addition, the inspector noted that the licensee

identified 22 Operating Instructions which were also revised to include

the precaution.

The inspector

sampled

seven of the identified

procedures

and verified that the procedures

included the precaution in

the latest revision.

The inspector also verified that Site Standard

Practice

SSP-12.1,

Conduct of Operations

was revised to ensure that

plant radiological personnel

are informed prior to evolutions

or

activities which .have the potential to significantly change radiological

conditions.

The inspector

noted that during the recent Unit 2 feedwater

temperature

reduction,

the licensee

used caution orders to ensure that

Radcon

personnel

were contacted prior to operating heater extraction

steam

isolation valves

so that Radcon could evaluate radiological conditions.

The inspector concluded that the licensee's

actions were adequate.

This

violation is closed.

II. Maintenance

Ml.1

Conduct of Maintenance

Scaffolds

and

Tem orar

Platforms

Ins ection Sco

e

62707

On August 26,

1997, the inspector

examined

20 scaffolds/platforms

located in the Unit 2 reactor bui.lding.

The scaffolds/platforms

were

reviewed with regard to the requirements

in Technical Instruction

O-TI-264, Scaffolds

and Temporary Platforms.

The inspector

focused

on

.verification of proper clearance

between the scaffolds

and safety

related equipment.

~

~

lj

0

b.

Observations

and Findin s

During the course of the revi ew, the inspector identi fied several

specific examples

in which the procedural

guidance

was not being

correctly followed.

Additionally, the inspector noted at least

one

issue in which the procedural

expectations

appeared to be not realistic

and were not being applied.

Several

problems with the procedure

were

also identified.

General

precaution 4.4 and step 7.11.4 of 0-TI-264 require that

areas

around scaffolds which can be used for handholds

or

footholds shall

be posted with caution signs and/or tape to avoid

use

as handholds

or footholds.

The erecting

foreman is supposed to

review and verify this when he signs the permit.

The inspector

did not observe

any such marking of potential

handholds or

footholds.

In the case of scaffold 2575-02,

a conduit going into

junction box 73-0111

was bent slightly and appeared

to have been

stepped

on.

These procedural

requi rements apparently

are related

to commitments

made to the

NRC as part of Licensee

Event Report

260/89-006.

In that event,

personnel

climbed on a reactor

protection system breaker

cabinet to access

a scaffold.

Appendix

H (Scaffold/Temporary Platform Erection Checklist) of 0-

TI-264 references

steps 2.6.7

and 2.7.6 of Appendix L (Seismic

Qualifications of Scaffolding and Platforms in Class I

Structures).

There is currently no step 2.6.7 in Appendix L and

step 2.7.6 does not address

clearance

issues.

It appeared that

the correct reference

would be step 2.7.7.

Numerous

examples

were noted in which the Appendix

H checklist

indicated that the clearance

requirements

of Appendix L were met

but

a Site Engineering evaluation

(Appendix N) was completed to

address

deviations

from the clearance criteria.

The inspector

noted several

indications that the Appendix

N checklists

were not

being completed in a diligent manner.

Section 2.7.7 of the TI states

that if the clearance

requirements

can not physically be achieved,

Site Engineering evaluation

and

approval shall

be obtained

and documented

on Appendix

N prior to

erecting the portion of the scaffold in which the clearance

cannot

be achieved.

The inspector noted that actual practice is to

complete the site engineering evaluation in parallel with or after

the scaffold is built.

While no scaffolds were found with expired tags,

the inspector

noted that the expiration dates

were often set far past expected

end of work activities.

For example.

most of the refueling outage

scaffolds

had expiration dates of December

31,

1997. Apparently,

the scaffolds are being tagged this way due to a perception that

there

may be delays in removing all the scaffolds following the

outage.

45

The inspector

noted that in several

cases.

scaf'folds were built

with unnecessarily

small clear ances to safety related

equipment.

In most cases.

the deviations

were addressed

in site engineering

evaluations

as required.

However. larger clearances

could have

been physically achieved

and there did not appear to be

a need for

such close proximity to safety systems

(examples

included plating

located less than one inch from core spray

and

HPCI piping and

scaffolding very close to recirculation seal

pressure

sensing

lines).

The inspector

found

a scaffold board wired across

the stairwell in

the northwest corner

room.

While the board did not contain

a

formal scaffold permit,

an August 22 note was attached

indicating

that Operations

and Fire Protection personnel

had approved its

placement for use

on Sunday.

The board

had not been

removed after

Inservice Inspection activities were completed.

The inspector

immediately reported the issue to the Unit 2 control

room and the

board was

removed.

The inspector also discussed

Assistant Unit

Operator sensitivity to such issues with the Operations

manager.

Scaffold 2322 did not have the minimum clearance

stated in the

Appendix

N evaluation.

The inspector noted that

some scaffolding

tubing was very close to the torus

on one end with the other end

contacting

a concrete wall.

The engineering evaluation stated

that members pointed at the torus should have at least

4 inches of

clearance

from the torus.

This issue

was immediately reported to

the Unit 2 supervisor

and the scaffold was

removed later that

evening.

Problem Evaluation Report

(PER) 971339 was initiated.

The scaffold had been erected

in February

1997 for work completed

some time ago.

Additionally, the Appendix

M checklist was not

filled out for this scaffold.

Scaffold 2720 did not have

a field engineer

review documented

on

the 'tag.

Step 7. 11.8 of the TI appeared

to require this. Scaffold

2733 had no expiration date

on the tag.

Scaffold 2575 was located very close to residual

heat

removal

piping and instrument tubing associated

with HPCI and

recirculation

pumps.

A ladder for egress

was located'very close

to 2-LPNL-925-00078.

The site engineering evaluation did not

address all the clearance

deviations noted.

The inspector

noted

that conduit going to junction box 73-0111 appeared

to have

been

bent

as

a result of being stepped

on.

The conduit was located in

the path between the ladder to the scaffold.

Scaffold 2657 had three spray cans sitting on it that could have

fallen off. Additionally, the site engineering evaluation stated

that

a 1/2 inch minimum clearance

should be maintained.

'However,

some parts of the scaffold were closer than that to plant

equipment.

0

0

o

The inspector did not identify any of the scaffolds located

such

that it would adversely affect the operation of valves or

electrical

equipment.

However, in several

cases,

the

2 feet

minimum clearance

(stated in the TI) from a valve handwheel

was

not met and Operations

concurrence of the deviation was not

documented.

The inspector noted that the scaffold inspections

were consistently

completed

and documented

as required

by the TI.

On the evening of August 27, the Unit 2 support

AUO identified that

scaffolding had been erected (earlier that day) such that it was

blocking air flow between the room cooler and the 2A residual

heat

removal

pump.

The scaffolding boards

were removed

and

PER 971350 was

initiated.

The deficiencies

noted

above

appear

related to two causes.

There are

weaknesses

in portions of the procedural

guidance for scaffolding

erection,

and supervisory

personnel

are not ensuring that procedural

requirements

are satisfactorily met.

Violation 296/96-04-07,

Failure to Follow Procedural

Requirements

for

the Installation of Scaffolding,

was issued in May 1996.

The violation

had been

caused

by scaffolding constructed

too close to the switch for

an emergency diesel

generator field flash breaker.

This was the second

time that

a field flash breaker

had been inadvertently operated

during

egress

from a scaffold.

Corrective actions to the first instance

included requi ring verification and documentation that the three foot

clearance

requi rement

was met in the 0-TI-248 checklist

(Appendix M).

Corrective actions for the second incident included counseling of

scaffolding craft personnel

on the clearance

requi rements.

The

inspection

conducted this period indicated that the Appendix

M checklist

is not being rigorously completed.

Several of the above noted problems

involve noncompliance with the Appendix

M checklist.

The number of 'deficiencies indicate that involved maintenance

supervisors

are not enforcing high standards

of performance.

There have

been other

incidents within the last year at Browns Ferry involving

problems with oversight

and accountability

on the part of maintenance

supervision.

In May 1997, the

NRC identified problems with

implementation of Foreign Material Exclusion procedures.

In August 1996,

NRC inspectors identified poor oversight of painting activities

on the

Unit 3 emergency diesel

generators.

The licensee

has identified

examples of similar issues.

The deficiencies identified above are

a violation of TS 6.8. l.l.a, in

that procedures

for performing maintenance

that can affect safety

related

equipment

were not implemented correctly.

This issue is

identified as Violation 260/97-09-02,

Scaffolding Controls Not Properly

Implemented.

0

0

0

Conclusions

The inspectors identified that the licensee

was not properly

implementing procedural

controls over scaffolding.

In some cases',

scaffolds

near

safety related equipment

were not constructed

in

accordance

with limitations in the procedure

or in the required

engineering evaluation.

The scaffolding assembly checklist was not

being properly completed.

Some procedural

requi rements,

which would be

difficult to complete,

were not being implemented.

No safety systems

were rendered

inoperable

by the noted deficiencies.

The inspectors

concluded that the number

and nature of the deficiencies indicate that

supervisory personnel

are not enforcing standards

and failed to ensure

that procedural

requirements

are satisfactorily met.

Functional Testin

of Snubbers

Ins ection Sco

e

62707

61726

The inspectors

noted that the licensee

was performing functional testing

of safety system snubbers

as

a pre-outage activity. The inspectors

reviewed the applicable regulatory requirements,

procedures.

and work

instructions.

Observations

and Findin s

On September

9,

1997, the inspectors

noted that the licensee

had

removed

a mechanical

snubber

(2-SNUB-063-5001)

associated

with the Unit 2

Standby Liquid Control

(SLC) system from service to perform functional

testing.

The inspector

was aware that the Unit 2 SLC system

had been

removed

from service

on September

7 for planned maintenance

and returned

to service

on September

8.

The detailed work schedule

for the

SLC

inoperability period (referred to as

a fragnet by the licensee)

did not

include th'e snubber testing.

During the snubber work, the licensee

entered

a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> limiting condition for operation

and referenced

TS 3.6.H.l.

This practice

had been

implemented for snubber testing prior

to recent refueling outages

at Browns Ferry.

Snubbers

associated

with

the Unit 2 core. spray

and residual

heat

removal

systems

had also been

tested prior to this outage.

The inspector

reviewed Work Order

(WO) 96-015749 which contained the

work instructions

for the testing.

The inspector noted that the

WO

contained

statements

which indicated that the work was to be performed

as

a shutdown activity.

Technical Specification (TS) 4.6.H, which addresses

functional testing

of snubbers,

states that "During each refueling outage,

a representative

-sample of 10 percent of the total of each type of safety-related

snubbers

in use in the plant shall

be functionally tested either in

place or in a bench test."

Additionally, the TS bases

states that

snubber

operability tests shall

be performed during refueling outages,

at approximately

18-month intervals.

The inspector concluded that the

current

Browns Ferry TS directed that functional testing of snubbers

was

4~

0

Hl.3

10

to be performed while the unit was shutdown.

The inspector

immediately

informed maintenance

management.

Mechanical

snubber testing is performed in accordance

with Procedure

2-

SI-4.6.H-2A, Functional testing of Mechanical

Snubbers

(Revision 4).

The

inspector

reviewed the procedure.

Sections

1.2.2.2

and 1.3. 1 contain

statements

which indicate that the testing is to be performed in a

refueling outage.

However, sections

1.3.2 and 3.2.8 indicate that the

procedure

can be performed in other than outage conditions for snubbers

outside the drywell.

The inspector

concluded that the procedure did not

exclude functional testing at times other than

an outage.

Later on September

9, the licensee

informed the inspectors that

a review

had been completed

and it was determined that

TS requirements

had not

been

met regarding the snubber testing.

The licensee's

review

identified 1980 guidance

from the

NRC indicating that the TS for

. functional testing of snubbers

should indicate that the testing is to be

performed while shutdown.

The Browns Ferry TS for snubber testing

was

revised in 1982.

The licensee

indicated that

a

10 CFR 50.73 report

would be made addressing

the issues.

At the September

10,

1997,

Management

Review Committee meeting,

Problem

Evaluation Report

(PER) 971406 was reviewed.

The

PER addressed

the

snubber testing issue

and was assigned to Operations for resolution.

Snubber functional testing

was stopped.

Discussions with plant

management

indicated that the licensee

was reviewing other maintenance

activities to ensure that no similar TS noncompliances

existed.

Plant

management

also indicated to the inspector that the

PER resolution would

address

the issue of the

WO being worked at power although it was coded

as

a shutdown activity.

Functional testing of snubbers

at other than refueling outage conditions

is

a violation of TS 4.6.H.

This is identified as Violation 260/97-09-

01, Functional Testing of Snubbers

While Not in Refueling Outage

Conditions.

Conclusions

The current

Browns Ferry TS indicates that .functional testing of

snubbers

is to be performed in a shutdown condition.

The licensee

was

conducting the testing with the unit at power and on snubbers

for

systems

required to be operable.

Procedural

controls for the testing

did not enforce the TS requirements.

Hain Steam Line Tunnel

Tem erature

Switch Test Heatin

Coil Ad ustment

Sco

e

62707

The inspector

observed

maintenance activities to adjust the test 'heating

coil associated

with main steam line tunnel temperature

switch (TS)

3-TS-1-29C.

0

b.

Observations

and Findin s

11

During testing

on August 22,

1997,

a test deficiency was identified on

3-TS-1-29C when the temperature

switch failed to actuate

during the

performance of surveillance instruction 3-SI-4..2.A-f(A2), Hain Steam

Line Tunnel

High Temperature

Functional Test.

Channel

A2.

Temperature

switch 3-TS-1-29C was declared

inoperable.

The licensee

determined that

the test heating coil. used to actuate the temperature

switch.

needed to

be adjusted to move the coil closer to the switch.

On August 26,

1997.

~ the inspector

observed troubleshooting activities to adjust the test

heating coi 1 on temperature

switch 3-TS-1-29C.

The inspector attended

the prejob brief for the coil adjustment

conducted in the control

room.

Since this evolution was considered

high

risk, the group discussed

that no other testing would be performed which

could cause

a half scram while the activities were being accomplished.

The group discussed

that there would be

a possibility of a half scram if

the temperature

switch is loose when the coil adjustment

was

made

even

though there

was no indication that the switch was loose.

The team

considered

numerous

aspects of the job and the potential for problems to

the extent that responders

would be dressed

and available to immediately

attend to an injury in the high radiation area.

The inspector

considered that the licensee

was well prepared

for this task.

The inspector

observed the coil adjustment

from the video camera set

up

in the main steam tunnel.

The Instrument Haintenance technician

performed the adjustment

as planned

and swiftly with consideration

for

the high radiation area that was entered.

Following completion of the coil adjustment,

the licensee

performed

surveillance instruction 3-SI-4.2.A-8FT(A2), Hain Steam Line Tunnel

High

Temperature

Functional Test,

Channel

A2, to meet the surveillance test

interval requirement

and to post maintenance test the temperature

switch.

The temperature

switch actuated

when the test pushbutton

was

depressed

the fourth time.

The procedure

allows the test pushbutton to

be depressed

additional times to ensure that the temperature

switch

temperature

is raised

above the setpoint.

The inspector

noted that the

procedure

performance

appeared to be slightly cumbersome.

The Unit

Operator identified some potential

enhancements

which he indicated would

be submitted

on

a procedure validation review checklist.

The

temperature

switch was declared

operable

on August 26,

1997.

C3

EECW Pum

Im eller Ad ustment

Sco

e

62707

The inspector

observed

maintenance activities to reset the

pump impeller

clearance

on the

C3 Emergency

Equipment Cooling Mater

(EECW)

pump.

0

0

II

M8.2

M8.3

13

The emergency diesel

generator auto-started

as designed.

This

LER is

closed.

Closed

'Licensee

Event

Re ort

LER 260/96-002-00

Main Steam Isolation

Valves

Leak Rate

Exceeded

the Local

Leak Rate Test Acceptance Criteria

Due to Internal

Component

Wear.

This

LER was submitted

as

a voluntary

LER for information only.

On March 23 and 24,

1996, during

a Unit

refueling outage the "A" and

"C" inboard main steam isolation valves

(MSIVs) had

a leakage that exceeded

the local leak rate acceptance

criteria of 11.5 standard

cubic feet per

hour

(SCFH).

The as-found

leakage

was 18.7

SCFH and 32.0

SCFH respectively.

The cause of the

leakage

was determined to be misalignment of the valve mating seats

caused

by internal

component

wear.

The "A" MSIV was changed to a long-

nosed

poppet to provide

a guidance

mechanism to improve the alignment

on

the mating seats.

The valve was retested with a 6. 1 SCFH as-left

leakage.

Only one long-nosed

poppet

was available

and the "C" MSIV was

repaired

by lapping and cleaning.

The "C" MSIV was retested with a 1.51

SCFH as-lef't leakage.

The inspector

reviewed the

LER and Technical

Specification

(TS) surveillance

requirement 4.7.A.2.i concerning

MSIV

leakage.

The TS only requi res that the valves

be tested

once each

refueling outage.

If leakage

exceeds

11.5 SCFH, the valves

must be

repaired

and retested until the leakage

meets the acceptance criteria.

The inspector concluded that the licensee's

actions were in compliance

with the TS.

This issue

has

been

a generic problem at Boiling Water

Reactors.

The licensee

referenced

previous

LERs concerning this problem

in this

LER.

This

LER is closed.

Closed

Licensee

Event

Re ort

LER 259/96-003-00

All Eight Plant

Emergency Diesel Generators

Unexpectedly Auto-Started

From A Spurious

High Drywell Pressure

Signal.

This event

was discussed

in Inspection

Report 96-04.

This event occurred during installation of wiring for the

digital feedwater modification.

A fault was introduced into the

Emergency

Core Cooling System

(ECCS) logic while preparing

wires for

termination in panel

2-9-81.

The fault caused

a spurious, high drywell

pressure

signal in the logic, which in combination with the existing low

reactor

pressure

condition in Unit 2 resulted in the Engineered

Safety

Feature actuation.

The licensee

determined the root cause

was

inadequate

work planning.

The work plan was originally approved to be

worked with panel

2-9-81 deenergized.

The work plan was subsequently

revised to work with the panel

energized.

The inspector

reviewed the licensee's

incident investigation report for

PER 960378.

The licensee

determined that as the outage schedule

firmed

up the panel would remained energized

during the work.

This would allow

the panel

work to proceed while maintaining

ECCS equipment

and their

initiation logic available for requi red testing.

Revisions

were made

to the work plan to delete the requirement for a clearance/isolation

and

a note was

added to perform the work "hot."

The work plan was never

sent

back to planning for review.

At the time of the event the

electrician

was working alone inside the energized cabinet.

As part of

the corrective action the licensee

was to change the administrative

process for reviewing and rescoping of workplans

when revisions are

il~

Ik

Observations

and Findin s

12

On September

1,

1997, the licensee identified that the

C3

EECW pump flow

data taken during quarterly surveillance testing

was below the minimum

flow limit and the

pump was declared

inoperable.

The licensee

prepared

a work order

(WO) 97-008664-000 to adjust the impeller clearance.

On

September

3,

1997, the inspector

observed the maintenance

crew pre-job

briefing and associated

work.

The brief was well conducted with focus

on right train and component:

personnel

safety issues

were addressed;

general

housekeeping

and foreign material exclusion

(FME) was discussed;

and specifics of the step text work order were reviewed.

The mechanical

maintenance

workers conducted

the job using portions of

MCI-0-023-PMP002,

Emergency

Equipment Cooling Water

and Residual

Heat

Removal Service Water

Pump (Byron Jackson

Type KX) Disassembly,

Inspection.

Rework and Reassembly.

The workers were knowledgeable of

the task

and the equipment.

Re lacement of 3-FCV-64-34 Solenoid Valve

Sco

e

62707

The inspector

observed

the replacement of the solenoid valve in the

control,circuit for the 3-FCV-64-34 valve.

The licensee

determined that

the failure of the 3-FCV-64-34 valve to close

upon

demand

was due to the

solenoid valve in the control circuit not operating properly.

Observations

and Findin s

On August 28,

1997, the inspector

observed the replacement of the

ASCO

solenoid valve used to control the 3-FCV-64-34 valve.

The repair

evolution was well planned

as

a contingency if testing concluded that

the

ASCO solenoid valve was the cause of the 3-FCV-64-34 valve fai lures.

The inspector did not identify problems with the maintenance

work.

Conclusion

The inspector

concluded that the maintenance

work observed

during the

inspection period was generally well planned

and worked.

The inspector

considered that ALARA planning of contingencies

was good with regard to

the high radiation evolution observed.

A strong prejob brief was

evident in preparation for C3 emergency

equipment cooling water

pump

work.

Miscellaneous

Maintenance

Issues

(62707,

92902)

Closed

Licensee

Event

Re ort

LER 259/96-002-00

An Emergency Diesel

Generator Auto-Started

Due To Undervoltage Condition As A Result of

Personnel

Error.

This item was previously discussed

in Inspection

Report 96-04.

The inspector

reviewed the

LER and the description of the

event was the same

as in the Inspection Report.

This event

was caused

by a personnel

error.

Personnel

involved in the test were disciplined.

ll

0

0

14

made.

Upon further review, the licensee

determined that the existing

procedural

requi rements

were adequate

and did not require revision.

Site Standard

Practice.

SSP 6.2

~ Maintenance

Management

System,

requires

under step 3.5.2 that revisions to workplans

be sent to planning for

review.

This was not followed.

Since the procedure for contro1 of

workplans

was not followed this was

a violation of 10 CFR 50 Appendix B,

Criterion

V for failure to follow procedure.

This non-repetitive

licensee identified and corrected violation is being treated

as

a Non-

Cited Violation (NCV), consistent with Section VII.B.1 of the

NRC

Enforcement

Po1ic

.

(NCV 50-260,296/97-09-04,

Failure to Follow

Procedure for Workplan Revision).

The inspector concluded that the incident investigation report was

thorough

and comprehensive.

This

LER is closed.

H8.4

0 en

Ins ection Followu

Item

IFI

296/96-08-03

Unit 3 Main Steam

Isolation Valve (HSIV) Circuitry Failures.

Inspection

Reports

96-05 and

96-08 describe

NRC review of several

MSIV limit switch fai lures

and the

licensee's

corrective actions which included installation of temporary

modifications.

The inspector

reviewed Revision

2 of Problem Evaluation

Report

(PER) 96-0083.

During the most recent Unit 3 refueling outage,

the problem was traced to damaged insulation

on conductors in Conax

conduit assemblies

and the situation was corrected.

It was concluded

that the Kapton insulation

on the conductors

was

damaged

because

heat

shrink polyolefin tubing had not been installed

on the inboard

conductors

during installation.

The

PER noted that

NRC Information Notice (IN) 88-89 addressed

this concern.

The inspector

reviewed the

IN

and noted that it specifically addressed

the use of the polyolefin

.tubing to mechanically protect Kapton insulation.

The licensee

attributed the fai lure to install the heat shrink to a lack of specific

guidance in work and vendor documents

and workers not understanding

some

of the instructions.

Similar maintenance activities have

been completed

in the past properly.

The licensee

implemented corrective actions to

ensure workers will understand

the importance of installing the heat

shrink on the inboard conductors.

The licensee

determined that

a total

of 69 similar seals exist on Unit 3 and has selected

10 percent

(7) of

these seals to inspect during the upcoming outage to determine if heat

shrink was applied to the inboard conductors.

No similar failures have

occurred

on Unit 2.

Pending results of those inspections,

the IFI

remains

open.

,

H8.5

Closed

Violation 296/96-04-07,

Failure to Follow Procedural

Requirements

for Installation of Scaffolding.

Section Hl. 1 describes

NRC inspection of scaffolds in the Unit 2 reactor building.

Numerous

deficiencies

were identified and cited as Violation 260/97-09-02.

Additional reviews of scaffolding controls will be performed

as followup

to Violation 260/97-09-02.

Violation 296/96-04-07 is closed.

0

0

Cl

15

El

Conduct of Engineering

III. En ineerin

El. 1

C.

E2

E2.1

RHRSW/EECW

Pum

Flow Test Data

Used for In-Service Testin

Trendin

Sco

e

37551

61726

The inspector

questioned

flow data

used to support In-Service Test

trending

on the residual

heat

removal service water and emergency

equipment cooling water

(EECW) pumps.

Observations

and Findin s

The 1-icensee

performs

a quarterly flow test

by adjusting discharge

pressure to 135 psig and reading

mV from an input to a flow modifier.

The

mV reading is then

used in a calculation to determine the flow in

gpm.

The

C3

EECW pump trend curve shows what appear to be comparable

test results for flow over several

quarterly tests until the

September

1,

1997, test which shows that the

pump is in the inoperable

range

due to low flow:

A recent decrease

in flow during testing of the

83

EECW pump again represents

potential

inaccuracies

in pump testing

methodology.

The

B3

EECW pump was replaced with a new stainless

steel

impeller

and tested with flow very near the original baseline.

Twelve

days later, the

pump flow tested

approximately

200 gpm lower and put the

pump in the alert range which requi red increased

frequency testing.

Based

upon review of the examples identified and discussion with the

licensee,

the inspectors

determined that

pump testing allowed

inaccuracies

in the flow determination.

The licensee indicated that

they would pursue

more repetitive methods of obtaining

mV data for the

flow calculation.

Conclusions

Based

upon review, of the examples identified and after discussion with

the licensee,

the inspectors

concluded that the

pump testing

was limited

in its repeatabi lity.

The inspectors will review the licensee's

actions

under Inspection Followup Item (IFI) 50-260,296/97-09-07,

RHRSW/EECW

Pump Flow Testing Issues.

Engineering Support of. Facilities and Equipment

Pressurization

of Shutdown Coolin

Suction

Pi in

Sco

e

37551

71707

The inspectors

reviewed

and monitored the licensee's

actions

regarding

pressurization

of portions of the Unit 2 shutdown cooling suction

,piping.

Apparently,

a very small

amount of reactor coolant leakage

past

the shutdown cooling isolation valves

(2-74-47 and 48) was causing the

suction piping to pressurize to above

100 psig.

0

II

16

b.

Observations

and Findin s

In August, the licensee

became

aware that

a slow pressurization of

portions of the shutdown cooling

(SDC) suction piping outside the

containment isolation valves

was occurring.

Annunciator 2-XA-55-3E,

window 32,"RHR SYS I/II DISCH OR SD CLG HDR PRESS

HIGH" began to alarm

once every several

hours.

The annunciator

was alarming due to pressure

switch PS-74-93 sensing

100

sig.

This pressure

switch senses

shutdown cooling piping pressure

etween the outboard

SDC suction containment isolation valve and

SDC

suction isolation valves located near the

RHR pumps.

The control

room

operators

complied with the alarm response

procedure which included

actions

per section 8.30 of Operating Instruction OI-74 alarm response

procedure.

These actions

included venting/draining the line from inside

the drywell access

area to reduce the pressure.

There is

a relief valve

(74-659) located

on the line which is set to relieve pressure

at

150

psig.

Due to the potential safety significance of the condition. the

inspectors

monitored the licensee's

actions closely.

The licensee classified the issue

as

an .operator work around

and

repetitive alarm issue.

Significant engineering

and management

attention

was applied to investigation of the condition.

The inspectors

met with licensee

management

and engineers

several

times during the

report period.

Since the licensee's

leakage estimate via calculation

appears

to be well within local leakrate testing limits. the inspectors

focused

on verification that the licensee

was adequately

pursuing the

problems while plant conditions were such that the leak was present.

Completed

and planned actions discussed

included:

After assuring that procedures

would cause the

SDC suction. piping

to be refilled prior to it being placed in service,

the licensee

revi'sed section 8.30 of OI-74 such that

a larger volume of the

SDC

suction line was drained in response to the annunciator.

The

drain point was

moved to a fuel pool cooling system connection in

the corner

room above the

RHR pumps.

This increased

the interval

between draining evolutions

from several

hours to several

days.

The inspectors

walked down the revised procedure

flowpath and

identified no significant problems.

The licensee

confirmed that the Unit 2 SDC suction relief valve

(74-659)

had

a

150 psig setpoint

and was tested satisfactorily in

1993.

The licensee

also intends to test'the relief valve during

the upcoming refueling outage.

Controlled drawings indicate that

the

SDC piping is rated for 150 psig outside the containment

isolation valves.

Engineers

obtained temperature

measurements

on the piping and

conducted

other diagnostic reviews.

Previous local leakrate

testing of the 74-47 valve (outboard isolation) indicated that the

leakage

was

0 standard

cubic feet per hour.

The acceptable

0

Ih

17

leakrate of the 74-47 by Appendix J requirements

would be

a small

fraction of a gallon per minute of water (20 standard

cubic feet

per hour air).

The 74-47 also fulfills a pressure

isolation

function.

Acceptable leakrate for that function (1/2 capacity of

relief valve) would be 10.5 gpm,

The licensee's

estimate of the

resent leakrate

was done by calculation

and indicated that it is

ess

than these limits.

The licensee ini'tiated

a Work Order to apply additional torque to

the handwheel of valve 74-47 to seat the valve better.

The torque

will be limited to ensure that the motor operator will still

operate that valve if needed.

The additional torquing had not

been

implemented at the close of the inspection period since the

revised draining method significantly increased

the time intervals

between

increased

pressure

indications.

During the outage.

the

torque switch setting of the 74-47 valve is scheduled to be

increased

as

a Generic Letter 89-10 enhancement.

The licensee'iscussed

the issue with similar facilities in order

to determine available

means of resolution.

Technical

Support developed

a resolution plan which includes

installation of pressure

recording instrumentation

and additional

temperature

measurements.

Refueling outage contingencies

being

considered

include

a modification to install

a controlled leakoff

line which could be used to port leakage

back to the torus.

c.

Conclusions

The inspectors

concluded that the licensee

was pursuing the problem in a

reasonable

manner

and the present conditions

do not represent

an

immediate safety concern.

Licensee

management

has indicated that the

intent is to effectively address

the issue

such that it will not exist

once the unit is returned to power after the refueling outage.

E8

Hiscellaneous

Engineering

Issues

(92903)

E8. 1

Closed

LER 296/96-004-00

LER 296/96-004-01

LER 296/96-004-02

and

LER 296/96-006-00

Loss of the Emergency

Core Cooling Systems

(ECCS)

Division I and Division II Instrumentation

Renders

ECCS Equipment

Inoperable.

These four LERs addressed

fai lures of the

ECCS inverters

which occurred in 1996 due to failures of silicone rectifiers

and

a

shorted

commutation capac'itor.

Inspection

Followup Item (IFI) 296/96-

08-02,

ECCS Inverter Failures,

addressed

these

problems.

Detailed

inspector

review and closeout of the IFI is addressed

in Section

E8.1 of

Inspection Report 97-07.

The LERs are closed.

E8.2

Closed

Licensee

Event

Re ort

LER 296/96-003-00

Unit 3 Scram

On Low

Reactor

Water Level

Due To Failure Of The Steam

Packing Exhauster

Bypass

Flow Control Valve.

This event was discussed

in Inspection Report 96-

05.

The initiating event for this scram was the valve shaft failure of

the steam packing exhauster

bypass

flow control. valve, 3-FCV-2-190.

The

il

0

0

18

valve failed close causing

reduced

condensate

flow and tripping of

feedwater

and condensate

booster

pumps.

This resulted in low reactor

water level

and

a reactor

scram.

The cause of the valve failure was due

to a material defect in a notched sensitive

area.

The licensee

replaced

the air operated

valve with a manual

valve following the event.

The

inspector

reviewed the Inspection Report

and

LER.

The inspector

looked

at the valve in the plant .and the valve had been replaced with a motor

operated

valve.

This

LER is closed.

Closed

Licensee

Event

Re orts

LERs

260/96-004-00

260/96-004-01

260/96-008-00

260/96-008-01

and 260/95-003-02

Main Steam Safety/Relief

Valves

Exceeded the Technical Specifications

Required Setpoint Limit as

a Result of Oisc/Seat

Bonding.

All of these

LERs concern the same issue

of setpoint tolerance drift.

Setpoint drift is

a generic concern in

Boiling Water Reactors

using Target

Rock Two-Stage Safety Relief Valves

(SRVs).

The cause

has

been attributed to corrosion bonding of the

SRV

pilot disc/seat

interface resulting in drifting of the

SRV setpoints.

The licensee

had previously implemented

a

BWR Owners Group

recommendation

for 3 of the

13 SRVs.

This recommendation

was to replace

the

SRV cartridges with cartridges that have

a platinum alloyed ste11ite

pilot disc.

However, test results

showed that the

SRVs with the

platinum alloyed stellite discs experienced

setpoint drift comparable to

the

SRVs with stellite discs.

Therefore the licensee is continuing with

long 'term corrective action to resolve this issue.

The licensee's

analysis for a limiting pressurization

transient

concluded that even if

four SRVs completely failed to open

and the remainder operated

at ten

percent

above setpoint

a safety limit would not be exceeded.

Although

the conditions reported in the

LERs were conditions outside Technical

Specification they were bounded

by analysis.

In LER 296/97-003-00

concerning the same issue for Unit 3, the licensee

discussed

installing

pressure

switch actuation for the SRVs.

This modification has

successfully

been installed at another facility.

This modification is

planned for Unit 2 during the next refueling outage.

Additiona] actions

are being evaluated, in connection with the Boiling Water Reactors

Owners

Group.

LER 296/97-003-00

remains

open to track final resolution of this

issue.

The previous

LERs are closed.

Closed

Unresolved

Item 260/97-07-04

Failure of Fuel

Pool Cooling

Pump.

This item addressed

the failure of the

2B fuel pool cooling pump

due to cavitation.

IR 97-07 describes

NRC review of the event.

The

inspector

reviewed

Problem Evaluation Report

(PER) 970946 which

addressed

this issue.

The inspector

concluded that the licensee's

corrective actions sufficiently addressed all the deficiencies

associated

with the incident.

The inspector questioned

the scheduled

completion dates

(August 1999) for Site Engineering to issue design

changes to prevent fuel pool cooling pump cavitation when the

demineralizer

bypass

valves

opened.

Subsequently,

the inspector

was

informed that management

intends to implement the design

changes

sometime after the Unit 2 refueling outage,

most likely during the late

fall or winter months.

As noted in IR 97-07, the system engineer

and

his supervisor failed to initiate a

PER on the cavitation problem when

19

are that

a

PER be initiated on such

an incident.

This non-repetitive,

licensee

identi fied and corrected violati on is being treated

as

a Non-

Cited Violation (NCV), consistent with Section VII.B.1 of the

NRC

Enforcement Polic

.

NCV 260/97-09-05,

Failure of Fuel

Pool Cooling

Pump.

The unresolved

item is closed.

E8.5

Closed

Unresolved

Item URI 50-260/97-08-02

Incorrect Oil Used in Two

EDGs.

The URI addressed

the failure of the licensee to promptly

identify that zinc additive oil had been put in the

2A EDG.

This

failure led to the incorrect oil also being put into the

2D

EDG

approximately four months later.

The immediate corrective actions to

drain and refill the oil in the

2A and

2D EDGs were discussed

in NRC IR

97-08.

After replacing the oil. the zinc content values for the two

EDGs were substantially

decreased;

however, the zinc content

was still

above the required level. Subsequent

actions

included partially draining

'nd refilling the

ZA and

2D EDGs in an attempt to decrease

the zinc

content further.

The licensee is actively pursuing the higher than

allowed zinc levels.

In March 1997,

problem evaluation report

(PER 970563)

was initiated to

address

a third party audit finding that "engineering

component testing

program weaknesses

could delay resolution of known equipment

problems

and result in equipment

problems not being identified prior to failure."

This included that "the lubricating oil analysis results

are not

reviewed or trended...as

an aid in predicting equipment performance."

Corrective actions for the identified problem are not complete.

On September

11,

1997. the licensee briefed the inspector

on current

plans to upgrade the program to track lube oil samples.

The Plan of the

Day meeting materials will have

a status of the oil samples

once per

week.

The licensee

has also

named

a point of contact

on site for the

lube oil analysis

program.

Currently, the licensee is using chemistry

instruction (CI) CI-130, Diesel

Fuel

and Lube Oil Monitoring Program, to

implement 'the lube oil program;

however, the licensee

plans to

incorporate

lube oil guidance into Technical Instruction (TI) TI-230.

Additional planned corrective actions include establishing criteria for

each

component which will be incorporated into the procedure

and

. personnel

training in performing evaluation of lube oil analysis

results.

The corrective actions are planned for implementation

by

December

19,

1997.

The inspector concluded that the planned corrective

actions are adequate.

This non-repetitive licensee identified and corrected violation is being

treated

as

a Non-Cited Violation (NCV), consistent with Section VII.B.1

of the

NRC Enforcement Polic

.

The fai lure of the licensee to identify

that zinc additive oil had been put in the

2A EDG which led to the

incorrect oil also being put into the

2D

EDG approximately four months

later is identified as Non-Cited Violation (NCV) 50-260/97-09-03,

Incorrect Oil Used in Two EDGs.

0

S3

S3.1

20

IV. Plant

Su

ort'ecurity

and Safeguards

Procedures

and Documentation

Securit

Pro

ram Plans

Ins ection Sco

e

81700

The inspector

reviewed appropriate

chapters of the licensee's

Physical

Security Plan

(PSP)

and Safeguards

Contingency

Plan

(SCP),

Revision 1,

dated

October

19,

1995; Revision 2, dated February

29,

1996: Revision 3,

dated

May 13,

1996.

The inspector

also reviewed Revision 21, dated

April 14,

1995,

and Revision 22. dated

December

28,

1995, of the

Security Personnel

Training and Qualification (T&Q) Plan

and security

procedures

as listed in paragraph

S3.1(b).

Observations

and Findin s

Review of the changes

submitted to the

NRC in Revision l. 2,

and 3, of

the .PSP

and Revisions

21 and 22 of the

T&Q Plan for approval verified

that the

PSP

and

T&Q changes

as submitted were in compliance with the

requi rements of 10 CFR 50.54(p).

The

PSP changes

were mostly

administrative in nature with the exception of Revision 3, of the

PSP

which deleted the security requi rements

during the security upgr ade

project.

The

PSP changes

were well written and did not require any

additional clarification.

Physical Security Instruction Hanual

(PSIH),

Section

105,

was reviewed

and considered

acceptable

as guidance to

implement the l.icensee's

compensatory

measures

for inoperative active

vehicle barriers.

The procedure

required that inoperative active

barriers

be compensated

for within 10 minutes.

Section

105. of the PSIH

guidance stated that "a vehicle of at least

3 tons or higher be provided

in front of a non-functioning active vehicle barrier."

Additionally,

the inspector

reviewed

PSIH. Section

105, Security Testing

and

Haintenance

and found the licensee

had included the proper testing

and

maintenance

requi rements.

Conclusion

A random review,of plans,

records,

reports,

and interviews with

appropriate individuals verified that security plan and procedures

changes

did not decrease

the effectiveness

of the

PSP.

The inspector

reviewed Revision 1, 2,

and 3. to the

PSP

and Revision

21 and

22 of the

T&Q Plan and concluded that the

PSP

and

T&Q Plan changes

as submitted,

met the requirements of'0 CFR 50.54(p).

There were no violations of

regulatory requi rements

noted in this area.

il

0

0

S6

S6.1

21

Security

Or ganization

and Administration

Mana ement

Su

ort

Ins ection Sco

e

81700

The inspector

evaluated

the degree of the licensee's

management

support

to the Physical Security Program.

Based

on the requirements

contained

in the

PSP,

the inspector

reviewed the licensee's

Safeguards

Event Log

(SEL) entries.

This review was to determine if the licensee

appropriately assigned,

analyzed,

and set priorities for corrective

action for the reports

and log entries,

and whether the corrective

action taken

was technically adequate

and timely.

Observations

and Findin s

The licensee

had an on-si.te physical protection system

and security

organization.

Their objective was to provide assurance

against

an

unreasonable

risk to public health

and safety.

The security

organization

and physical protection system were designed to protect

against the design basis threat of radiological sabotage

as stated in

10 CFR 73. 1(a).

A proprietary security force provided site security for

the licensee.

At least

one full-time manager of the security

organization

was always on-site.

This individual had the authority to

di rect the physical protection activities of the organization.

The

management

system included

a mechanism

for establishing,

maintaining,

and enforcing written security procedures.

Licensee

management

exhibited

an awareness

and favorable attitude toward physical protection

requirements.

This was evident by the support that security was

provided in preparation for the Operational

Safeguards

Response

'valuation

(OSRE) which was successfully

completed

on May 8,

1997,

and

the continued outstanding

maintenance

and engineering

support to

maintain

and enhance security equipment.

The review of the SELs as of June

1997 indicated the following:

EVENTS

4th Quarter

'96

.

2nd Quarter

'97

1st Quarter

'97

Human Errors

Hardware Systems

Other Events

TOTALS

12 (11K)

97

(88%)

109 (100K)

03 (5C)

54 (95K)

57 (100K)

15 (17K)

74 (83K)

89 (100K)

Each quarter

had an excellent Trending Summary report that was provided

to site management.

4I

22

There were no long term compensatory

measures

in effect at the time of

the inspection.

Review of previous

compensatory

measures

indicated that

the licensee

had 2219 hours0.0257 days <br />0.616 hours <br />0.00367 weeks <br />8.443295e-4 months <br /> of compensatory

measures

in FY 1996.

Most

of the compensatory

measures

were in support of planned

outage of

equipment to support operations.

Review of the outstanding security

work-orders revealed the following:

~

0 High Priority orders

~

0 Medium Priority

~

19 Low Priority

Of the

19 outstanding security work-orders.

none involve regulatory

requirements.

Conclusion

The inspector

found that licensee

management

provided appropriate

and

excellent support for the Physical Security Program.

Examples of the

excellent

management

support were the support in preparation for the

OSRE and the continued engineering

and maintenance

support to maintain

the security equipment in a high state of readiness.

Additionally, as

'another

enhancement

the licensee is installing

a lightning dissipation

system to greatly eliminate lightning from striking the security

and

plant monitoring equipment.

There were no violations of regulatory

requirements

noted in this area.

Effectiveness of Mana ement Control

Ins ection Sco

e

81700

The inspector

evaluated

the adequacy of the licensee's

controls for

identifying, resolving

and preventing

problems

by reviewing such areas

as corrective action systems,

root cause

analyses,

and self-assessment

in the area of physical security.

Also, this inspection

was to

determine whether there were strengths

or weaknesses

in the licensee's

controls for the identification and resolution of the reviewed issues

that could enhance

or degrade plant operations

or safety.

Observations

and Findin s

To determine the adequacy of the above,

the inspector

reviewed the

,

licensee's

SEL entries.

This review was to determine if the licensee

appropriately assigned,

analyzed,

and set priorities for corrective

action for the reports

and log entries,

and whether the corrective

action taken

was technically adequate

and timely.

The root cause

analyses,

corrective actions,

and self-assessments.

as

mentioned in Paragraph

S6. 1,

above

and in Paragraph

S7. 1 below, were

reviewed

and found appropriate

and adequate.

II

Conclusion

23

S7

S7.1

The inspector

concluded that the licensee

evaluated the non-human

errors,

hardware

and mechanical

problems

and they were effectively

controlled and managed.

Quality Assurance in Security and Safeguards Activities

Audits and Corrective Actions

Ins ection Sco

e

81700

Based

on the commitments of the

PSP, the inspector evaluated

the

licensee's

audit program

and corrective action system.

This also

ensured

compliance with the requi rement for an'nnual

audit of the

security

and contingency programs.

During the inspection,

a small

representative

sample of the problems identified by audits

was evaluated

by the inspector to determine whether review and analysis

were

appropriately assigned,

analyzed,

and prioritized for corrective action

and whether the corrective action taken

was technically adequate

and

performed in a timely manner.

Observations

and Findin s

The licensee's

program commitments

included auditing its security

program,

including the Safeguards

Contingency Plan, at least every

12

months.

The audit included

a review of routine and contingency security

procedures

and practices.

This review evaluated

the effectiveness

of

the physical protection system testing

and maintenance

program.

This

annual audit was completed

on January

30,

1997.

and the results

are

documented in audit report SSA-9617.

The audit report was sent to the

site Vice President

and Corporate

Management.

Reports of audits were

available for inspection at the plant for a period of three years.

The

auditors concluded that the security program continued to meet the

regulatory requi rements.

In addition to the annual audits.

the licensee

had conducted audits of specific security practices

and the audit

findings were documented

in NA-BF-97-01, dated January

27,

1997;

NA-BF-97-11, dated February 25,

1997;

NA-BF-97-23, dated

March 31,

1997;

NA-BF-97-35, dated

May 6,

1997;

and NA-BF-97-46, dated June 3.

1997.

Conclusion

Licensee-conducted

audits were thorough,

complete,

and effective in

terms of uncovering weaknesses

in the security system,

procedures,

and

practices.

The last audit report concluded that the security program

was effective.

The licensee

had acted appropriately in response to

recommendations

made in the audit report.

The inspector determined that

audit items were reviewed. appropriately assigned,

analyzed,

and

prioritized for corrective action.

The corrective actions taken were

technically adequate

and performed in a timely manner

.

There were no

violations of regulatory requirements

noted in this area.

0

0

S.8

S8.1

S8.2

F2

24

Miscellaneous Security and Safeguards

Issues

(92904)

CLOSED

VIO 50-259 260 296/96-07-01,

Failure to Properly Search

Packages

Entering the Protected

Area.

The inspector

reviewed the

licensee's

lesson plan,

personnel

and package

search

enhancement,

and

the attendance

roster

and determined that all personnel

had been

retrained in proper search

procedures

as

a result of the incident.

The

inspector

reviewed search

procedures

during the inspection

and concluded

that 'personnel

were searching

packages

and containers

as required.

The

corrective action is considered

adequate

to close this violation.

CLOSED

IFI 50-259

260 296/96-07-02,

Lighting Glare Prevents

Adequate

Assessment

at the Intake Structure.

The licensee's

corrective actions

included re-positioning

and refocusing of cameras

25a

and 25b.

and hoods

were placed

on the cameras to prevent rain from landing on the lens

and

to shield direct light from the cameras.

Also. the light bulbs

on the

handrail

were changed to non-glare bulbs,

and the lens on'the high mast

lights were repositioned to reduce glare.

The inspector determined that

the corrective actions were adequate to close this IFI.

Status of Fire Protection Facilities and Equipment

Ins ection Sco

e

71750

62707

The inspector

observed

performance of section 7.2.8 of O-SI-4.11.8.1.C.

High Pressure

Fire Protection

System Flushes.

This section

addressed

portions of the Unit 2 reactor building preaction sprinkler system.

In

addition to assessing

the conduct of the test,

the inspector

examined

the strainer basket to determine if excessive quantities of corrosion

products or other materials

were entering the fire protection system.

Observations

and Findin s

The work was completed according to the work instructions.

The procedure

was actively uti1ized and the workers were knowledgeable of the

evolution.

Radio communications

were appropriately formal.

The workers

were careful

when draining the system to minimize overflow of the floor

drain.

Second party and independent verification were performed in

accordance

with requirements.

The workers were cautious

when re-opening

isolation valves.

The procedure directed that fire protection water be flushed (from the

outside loop header

into the reactor building and through the strainer)

for at least

10 minutes.

The strainer basket

was then inspected.

The

inspector

observed that the strainer contained only a thin film of

minute particles which could be easily wiped off.

There was not any

accumulati.on of corrosion products or other river materials in the

strainer or housing.

This indicated that the licensee's

processes

for

the raw water fire protection system are adequately protecting the

system.

IR 97-07 described

programmatic

review of the licensee's

program to,maintain the reliability of the fire protection

raw cooling

water

system.

0

25

R4

Staff Knowledge and Performance

in Radiological Controls

and Chemistry

R4. 1

Hi

h Radiation Area Doors

a.

Ins ection Sco

e

71750

During the inspection period, the inspectors verified that locked high

radiation areas

were maintained in accordance

with the licensee's

procedural

guidance.

b.

Observations

and Findin s

During tours of the facility, the inspectors

checked

numerous

locked

high radiation area

doors to verify that the doors were maintained

locked.

No problems were identified.

V.

Mana ement Meetin s

Xl

Exit Meeting Summary

The resident inspectors

presented

inspection findings and results to

licensee

management

on September

17,

1997.

Other formal meetings to

discuss

report issues

were conducted

on August

15 and September

8.

The licensee

acknowledged

the findings presented.

Proprietary

information is not included in this inspection report.

Licensee

PARTIAL LIST OF PERSONS

CONTACTED

T. Abney, Licensing Manager

,J. Brazell, Site Security Manager

R.

Coleman, Acting Radiological Control

Manager

J.

Corey, Radiological Controls

and Chemistry Manager

T. Cornelius,

Emergency

Preparedness

and Planning

C. Crane, Site Vice President,

Browns Ferry

R.

Greenman,

Training Manager

J.

Johnson,

Site (juality Assurance

Manager

R. Jones,

Assistant Plant Manager

S.

Kane, Acting Site Licensing Supervisor

G. Little, Acting Operations

Manager

D. Nye, Site Engineering

Manager

K. Singer,

Plant Manager

J. Schlessel,

Acting Maintenance

Manager

0

0

IP 37550:

IP 37551:

IP 40500:

IP 62707:

IP 61726:

IP 71707:

IP 71750:

IP 73756:

IP 81502:

IP 81700:

IP 92901:

IP 92902:

IP 92903:

IP 93702:

26

INSPECTION

PROCEDURES

USED

Engineering

Onsite Engineering

Licensee Self-Assessments

Maintenance

Observations

Surveillance Observations

Plant Operations

Plant Support Activities

Inservice Testing of Pumps

and Valves

Fitness

For Duty Program

Physical Security Program for Power

Reactors

Followup-Plant Operations

Followup-Maintenance

Followup-Engineering

Prompt Onsite Response to Events at Operating

Power Reactors

ITEMS OPENED

DISCUSSED

AND CLOSED

OPENED

~T

e

Item Number

VIO

50-260/97-09-01

VIO

50-260/97-09-02

NCV

50-260/97-09-03

Status

Open

Open

Closed

Descri tion and Reference

Functional Testing of Snubbers

While

Not in Refueling Out.age Conditions

(Section Hl.2)

Scaffolding Controls not Properly

Implemented

(Section Hl.l)

Incorrect Oil Used in Two EOGs

(Section E8.5)

NCV

50-260/97-09-05

Closed

URI

50-296/97-09-06

Open

IFI

50-260,296/97-09-07

Open

NCV

50-260,296/97-09-04

Closed

Failure to Follow Procedure for

Workplan Revision (Section H8.3)

Failure of Fuel

Pool Cooling

Pump

(Section E8.4)

Actions for Inoperable

Containment

Isolation Valve (Section Ol. 1)

RHRSW/EECW

Pump Flow Testing Issues

(Section El. 1)

DISCUSSED

T~e

Item Number

IFI

296/96-08-03

Status

Open

Descri tion and Reference

Unit 3 Hain Steam Isolation Valve

(MSIV) Circuitry Failures

(Section

M8.4)

il~

0'

27

0

~T

e

Item Number

'ER

296/96-002-00

VIO

296/96-12-01

VIO

296/96-13-03

LER 259/96-002-00

LER

260/96-002-00

VIO

50-296/96-04-07

LER 296/96-004-00

LER

296/96-004-01

LER 296/96-004-02

LER

296/96-006-00

LER 296/96-003-00

LER

260/96-004-00

260/96-004-01

260/96-008-00

260'/96-008-01

260/95-003-02

Status

Closed

Closed

Closed

Closed

Closed

Closed

Closed

Closed

Closed

Closed

Descri tion and Reference

Unit 3 Scram Following Loss Of

Reactor

Feedpump

3C (Section 08. 1)

Failure to Ensure

Proper Position of

EDG Aux Board

Room Exhaust'ans

(Section 08.2)

Uncontrolled Locked High Radiation

Area

(LHRA) (Section 08.3)

An Emergency Diesel Generator Auto-

Started

Due To Under voltage

Condition As A Result of Personnel

Error (Section M8.1)

Main Steam Isolation Valves Leak

Rate

Exceeded

the Local Leak Rate

Test Acceptance Criteria due to

Internal

Component

Wear (Section

M8.2)

All Eight Plant

Emergency Diesel

Generators

Unexpectedly Auto-Started

From A Spurious

High Drywell

Pressure

Signal

(Section M8.3)

Failure to Follow Procedural

Requirements

for Installation of

Scaffolding (Section

M8.5)

Loss of the Emergency

Core Cooling

Systems

(ECCS) Division I and

Division II Instrumentation

Renders

ECCS

Equipment, Inoperable

(Section

E8.1)

Unit 3 Scram

On Low Reactor Water

Level

Due To Failure Of The Steam

Packing

Exhauster

Bypass

Flow

Control Valve (Section E8.2)

Main Steam Safety/Relief Valves

Exceeded

the

TS Required Setpoint

Limit as

a Result of Disc/Seat

Bonding (Section E8.3)

(

0

URI

260/97-07-04

Closed

URI

260/97-08-02

Closed

IFI

259,Z60,Z96/96-07-02

Closed

VIO

259,260,296/96-07-01

. Closed'8

Failure of Fuel

Pool Cooling

Pump

(Section E8.4)

Incorrect Oil Used in Two EDGs

(Section E8.5)

Failure to properly search

packages

(Section S8.1)

Lighting glare hampered

assessment

at intake structure

(Section S8.2)

ik~

il~