ML18038B610

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Insp Repts 50-259/95-64,50-260/95-64 & 50-296/95-64 on 951119-951230.Violations Noted.Major Areas Inspected: Operations Which Included Unit 3 Restart,Review of Biological Shield Block Removal Practices,Fire Protection
ML18038B610
Person / Time
Site: Browns Ferry  
Issue date: 01/29/1996
From: Lesser M, Wert L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18038B608 List:
References
50-259-95-64, 50-260-95-64, 50-296-95-64, NUDOCS 9602120066
Download: ML18038B610 (60)


See also: IR 05000259/1995064

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W., SUITE 2900

ATlANTA,GEORGIA 30X94199

Report Nos.:

50-259/95-64,

50-260/95-64,

and 50-296/95-64

Licensee:

Tennessee

Valley Authority

6A 38A Lookout Place

1101 Harket Street

Chattanooga,

TN

37402-2801

Docket Nos.:

50-259,

50-260,

and 50-296

License Nos.:

DPR-33,

DPR-52,

and

DPR-68

Facility Name:

Browns Ferry Units 1, 2,

and

3

Inspection. Conducted:

November

19 - December.

30,

1995

Inspector:

eo ar

.

e

,

r.,

endor

ess

ent

nspector

a e

sgne

Approved by.

J.

Hunday,

Resident

Inspector

R. Husser,

Resident

Inspector

H. Horgan,

Resident

Inspector

R. Aiello,

DRS Inspector

(paragraph

2.2)

P. Byron, Resident

Inspector,

Brunswick (paragraph

2.2)

L. Garner,

DRP Project Engineer

(paragraph

2.2)

H. Janus,

Resident

Inspector,

Brunswick (paragraph

2.2)

R. Kopriva,

DRP Project Engineer,

Region

IV (paragraph

2.2)

C. Patterson,

Senior Resident

Inspector,

Brunswick (paragraph

2.3)

T. Tongue,

DRP Project Engineer,

Region III, (paragraph

2.2)

//z~/FI,

'r

.

esser,

>e

Reactor Projects

Branch

6

Division of Reactor Projects

ate

tgne

SUHHARY

Scope:

Inspections

were conducted

by the resident

and other inspectors

in the areas

of operations

which included the Unit 3 restart,

review of biological shield

block removal practices,

and several fire protection issues;

maintenance

whi'ch

included routine observations,

post maintenance

testing issues,

deficiencies

Enclosure

2

9602120066

960l29

PDR

ADOCK 05000259

8

PDR

f

il

associated

with a freeze seal,

4160 volt breaker work activities,

and review

of open items; engineering

which included secondary

containment ventilation

damper failures,

narrow range torus water level issues,

and recirculation

pump

seal

purge effects

on the nuclear heat balance calculation; plant support,

and

review of NRC Operational

Assessment

Team findings.

The inspection of the

Unit 3 restart

included continuous

NRC control

room monitoring for a period of

about two weeks.

Results:

Plant

0 erations

Unit 3 was started

up during this report period after being shutdown for about

ten years.

Throughout the startup,

strong

management

involvement was noted.

Overall, equipment

problems

were minimal.

Although

a small .number of

personnel

performance

and procedural

problems occurred,

the issues

were

limited and addressed

promptly.

No multiple unit operation or "wrong

component"

issues

were noted during the entire startup.

(Paragraph

2.2)

Several

deficiencies

involving fire protection issues

were identified:

A violation was identified:addressing

two problems associated

with fire

protection program equipment.

Although the underlying causes

of the two

instances

were different, both resulted

in fire 'protection

equipment

being inoperable without compensatory

actions.

(Violation 296/95-64-01,

Fire Protection

Program

Equipment Inoperable Without Compensatory

Actions, paragraph

2.6).

A non-cited viol'ation was identified due to

a fire watch not performing

his duties

as required

by procedures.

(NCV 50-296/95-64-04,

Inattentive

Fire Watch,

paragraph

2.8).

ll

An unresolved

item was identified during followup review of'n ORAT

finding.

Procedural

requirements

for control of ventilation systems

in

the event of a fire appear to insufficiently incorporate

statements

in

the Fire Protection

Report.

(Unresolved

Item 260,296/95-64-08,

Fire

Damper Procedural

Controls,

paragraph

6. 1).

A non-cited violation was identified when control

room operators

did not

position the high pressure

coolant injection flow controller switch as

required

by a checkl'ist.

Operabil'ity of the system

was not affected.

(NCV

296/95-64-05,

HPCI Flow Controller Switch not In AUTO, paragraph

2.3).

During 'review of ORAT findings,

a non-cited violation was identified

associated

with control

room operators

not logging information required

by

procedures

to be logged.

(NCV 296/95-64-07,

Failure to Record Information in

Unit Logs,

paragraph

6.2).

II

0

Haintenance

A non-cited violation was identified involving deficiencies during thawing of

a freeze seal.

Coordination

and communications

between

Operations

and

Haintenance

personnel

were not satisfactory.

Furthermore,

Haintenance

workers

did not perform procedure

actions sequentially.

(NCV 296/95-64-02,

Deficiencies Involving Control of Freeze

Seal,

paragraph

3.2).

A non-cited violation was identified which addressed

several

examples of

failure to complete post maintenance

testing prior to returning equipment to

service.

Good Operations

and Haintenance

management

actions

were noted in

identification and investigation of the issues.

(NCV 296/95-64-03,

Equipment

Returned to Service Without Proper

PHT Completion,

paragraph 3.3).

During observation of snubber maintenance,

minor problems

were identified with

the applicable

procedures

and the use of the procedures.

(IFI 260,296/95-64-

11, Thread Lubricant Effects

On Torque Values,

paragraph

3. 1).

During review of ORAT findings,

a non-cited violation was identified involving

instances

in .which personnel

did not adequately

implement requirements

for

procedural

revisions during testing or maintenance activities.

(NCV 296/95-

64-06, Failure to Follow Requirements

for Procedure

Changes,

paragraphs

6.3

and 6.4).

En ineerin

Supervision of the Unit 3 power ascension

testing

was strong.

The overall

solid personnel

and equipm=iit performance

resulted

in the completion of the

testing

program well ahead of schedule.

Additionally, it was noted that the

licensee's

application of lessons

learned

from the Unit 2 Restart,

regarding

flexibility in scheduling of testing activities, resulted

in an efficient test

program.

(paragraph

2.2).

Several

failures of secondary

containment ventilation system

dampers

due to

solenoid failures

have occurred

over the last several

months.

The licensee

has

been adequately

pursuing the root cause

and long-term resolution of the

problems.

During review of a recent

damper failure, the inspectors

questioned

short-term operability of similar dampers.

The licensee

subsequently

initiated replacement

of critical damper solenoids

on an accelerated

schedule.

(Inspector

Followup Item 260,296/95-64-10,

Secondary

Containment Ventilation

Damper Failures,

paragraph

4. 1).

A non-cited violation was identified involving errors in a calculation for the

setpoints of narrow range torus water level indication.

This error had

occurred

several

years

ago

and the overall safety significance

was small.

(NCV 260/95-64-09,

Violation of Torus Water Level TS, paragraph 4.2).

Plant

Su

ort

Improvements

were noted involving a previously identified access

control

weakness.

(paragraph

5).

0

II

REPORT DETAILS

Acronyms used in this report are defined in paragraph

8.

1.0

PERSONS

CONTACTED

Licensee

Employees:

Brazell R., Site Security Manager

Coleman R., Radiological Controls Manager

Corey J.,

Chemistry .and Radiological Controls Manager

Cornelius

T

,

Emergency

Preparedness

Manager

  • Crane C., Assistant Plait Manager
  • Johnson J., Site equality Manager

Jones

R., Unit 3 Startup

Hanager

  • Little. G., Operations

Superintendent

  • Hachon R., Site Vice Presi'dent,

Browns Ferry

Haddox J.,

Maintenance

and Modification Manager

Moll R., Plant Operations

Manager

Pierce

G., Technical

Support

Manager.

Preston

E., Plant Manager

Sabados J.,

Chemistry Manager

Salas

P., Licensing Manager

Shriver T., Nuclear Assurance

and Licensing Hanager

Wetzel S., Acting Compliance Licensing Manager

  • Williams H

, Engineering and'aterials

Manager

Other licensee

employees

contacted

included office, operations,

engineering,

maintenance,

and chemistry/radiation

personnel..

2.0

PLANT OPERATIONS (71707,

71715,

92901,

40500)

2.1

OPERATION STATUS AND OBSERVATIONS

Unit 2 operated

at power during this inspection period.

Unit 3 was restarted

after an extended

shutdown.

Paragraph

2.2 discusses

NRC review of the startup

which included continuous control

room monitoring.

Some inspections

were

condu'cted

on day and night shifts, during weekdays

and

on weekends.

Observations

included control

room manning,

access

control, operator

professionalism

and attentiveness,

and adherence

to procedures.

Instrument

readings,

recorder traces,

annunciator

alarms, operability of nuclear

instrumentation

and reactor protection

system channels,

availability of power

sources,

and operability of the Safety Parameter

Display System were

monitored.

Daily di'scussions

were held with plant management

and'arious

members of the

plant operating staff.

One of the inspectors

attended

the daily Plan of the

Day meetings.

Routine plant tours were performed throughout the reporting

period.

Observations

included valve position

and system alignment,

snubber

and hanger conditions,

containment isolation alignments,

instrument readings,

~

2'.3

HPCI

FLOW CONTROLLER SWITCH NOT IN CORRECT POSITION

On November 23,

1995,

an

NRC inspector noted that the

HPCI flow controller was

in, BALANCE instead of AUTO.

HPCI was operable

at this time having completed

hot quick start test earlier in the day.

The inspector inquired about the

system status with a unit operator.

The operator

researched

the last

procedures

performed to be sure of the system status

and alignment.

Within

minutes,

the oncoming

SOS toured the control board

and inquired about the

same

switch position.

This occurred

independent of any discussion with the

-inspector

and was noted

as

a good observation

by the

SOS.

It was determined

that during the run of the HPCI, the switch should

have

been returned to AUTO.

There is

a procedural

step which requires

a signature attesting to this switch

position.

The switch was subsequently

returned to AUTO and the licensee

initiated

a

PER to document the problem.

This issue

was discussed

in subsequent

shift operations shift turnover

meetings

as

a significant problem since it was

a mispositioned

switch that had

been repositioned

by

a procedure requiring

a signature.

This problem was not

identified during the next shift turnover following, operation of HPCI.

Also

mentioned in the turnover meeting

as

a factor in not catching the error,

was

that only partial control board walkdowns were conducted

due to every operator

having specific tasks to do.

It was emphasized, that complete

board walkdowns

and reviews would be conducted

and the time to do it correctly would be

allowed.

The mispositioned, switch did not affect the operability of HPCI.

Inspectors

noted that this is the

same type controller used for the feed

pumps

and the

controllers, are routinely operated

in BALANCE instead of AUTO.

The reason for

running the feed

pumps in BALANCE is that

a failure of a controller will allow

quick shifting to manual.

This will shift to the last,setting before the

failure and possibly avoid

a transient.

One operator indicated that he

regarded

the two switch positions

as equivalent since the functioning of HPCI

was essentially

the

same.

This operator

was retrained

on procedural

compliance

aspects

of the issues.

The inspectors

concluded that corrective

actions

taken in response

to the mispositioned

HPCI switch were prompt

and'ppropriate.

This licensee-identified

and corrected violation is being treated

as

a Non-

Cited Violation, consistent with Section VII.B.I of the

NRC Enforcement

Policy.

This issue is addressed

as

NCV 296/95-64-05,

HPCI Flow Controller

Switch not in AUTOS

a

2.4

NODE SWITCH KEY NOT IN SMITCH

On November '20,

1995, with Unit 3 in the startup

mode

and at approximately

3 percent

power, the inspector

noted that the mode switch key was not

installed in the

mode switch.

The inspector brought this to the attention of

the operations shift manager.

Within 10 minutes,

the key was located in the

Unit 3 key locker and placed in the

mode switch.

The inspectors

were

concerned that, if required,

the

mode switch could not be placed in the

shutdown position without the key installed.

(One of the initial operator

actions following a-reactor

scram is to place the

mode switch in the shutdown

position).

The primary manual scram switches

were. operable

at -the time.

After additional questioning

the licensee verified that the mode switch could

not be repositioned without the key installed.

This m>tter represents

an

example of poor procedural

controls of a safety related

component.

Corrective

action for this matter involved preparing

a night order directing operators

to

keep the key in the

mode switch at all times during plant operation.

The

inspectors

considered

the licensee's

corrective actions, related to this matter

as adequate.

2.5

FAILURE OF RESIDUAL HEAT REMOVAL VALVE TO FULLY SHUT CAUSES

UNEXPECTED

REACTOR WATER LEVEL DECREASE

On November

18,

1995, with Unit 3 in cold shutdown

and operators

making final

preparations

for the restart of the unit, unexpected

reactor water level

decreases

occurred during the operation of RHR;valves associated

with shutdown:

cooling.

Specifically, at approximately

1: 10 a.m., control

room operators

were attempting to place loop II of RHR into the shutdown cooling mode of

operation

when reactor water level

began decreasing

(Loop II of RHR is

comprised of the

3B and

3D

RHR pumps).

The shutdown cooling flowpath to the

suction of the

RHR pumps is from the "A" recirculation loop, through the two

containment isolation valves

(74-48 and 74-47)

and one of the four pump

suction valves

(74-2

[RHR pump 3A], 74-13

[RHR pump 3C], 74-25

[RHR pump 3B],

and 74-36

[RHR pump 3D]).

When the operators

opened

74-47 and'8,

vessel

level decreased

from 34 inches to 24 inches over several

minutes.

'Initially,

it was thought that the decrease

was caused

by filling of the

RHR piping.

After several

more cycles of 74-47

and

48 and

an investigation

by shift

operations

personnel,

the problem was traced to leakage

through the 74-13

valve (the shutdown cooli"", suction to the

3C

RHR pump).

Because

the

3C

RHR

pump is in loop I of RHR which was aligned in "standby"

(ready for the

LPCI

mode of operation),

the valve between

the torus

and the

3C pump (74-12)

was

open.

The 74-13 leakage

permitted

a direct flowpath from the reactor vessel

(through the 74-12) to the torus.

The lowest reactor level reached

during

these evolutions

was

22 inches.

The setpoint for shutdown cool.ing

1'ow level

isolation is

11 inches with the top of active fuel located, at approximately

-165 inches.

Although 74-13 indicated fully closed

by remote indication,,an operator

was

able to operate

the valve's actuator

hand wheel

approximately

20 turns in the

closed direction.

This corresponded

to only a fraction of a turn on the valve

stem.

Valve 74-13 closes

on torque

and the close indication limit switch is

set for 2-5 percent

open.

Subsequent

to the event,

the licensee

determined

that the torque switch was set at

a low value within the vendor's

acceptable

range.

The torque switch setpoint

was increased

and valve was successfully

cycled

a number of times.

It should

be noted that 74-13 is not addressed

by

the licensee's

GL 89-10 or 10

CFR, 50 Appendix J programs.

Following the event,

the inspectors

performed

an extensive

review of control

room chart 'recorders,

logs,

and

SPDS data.. Although problem i'dentification

required several

cyclings of the 74-47

and

48 valves

and extensive

investigation,

the inspectors

concluded that operator

performance

was adequate

and procedures

were followed.

The matter

was documented

on

PER 95-1752 .with

corrective action assigned

to the maintenance

valve engineering

group.

hi

~$0

Immediate corrective actions

involved electrically stroking the other

3

pumps'hutdown

cooling suction valves

(74-2,

25,

and 36)

and then manually engaging

the valves to ensure

they had fully closed.

No problems with these

valves

were identified.

Other corrective actions to be performed in the near term,

are

as follows;

1) Revise procedure

ECI-0-000-HOV001, (Electrical Corrective

Instruction Maintenance for Limitorque Motor Operated

Valves), to include

steps

to electrically stroke the valve and manually verify that it has torque

seated.

Additionally, steps

are scheduled

to be added to ensure

torque switch

settings will be returned to the as-found setting

on non

GL 89-10 valves

following maintenance

(In the past,

the torque switches

were returned to

a

minimal setting following maintenance).

2) This matter is scheduled

be

reviewed with plant maintenance

personnel.

3) Valve engineering

personnel

are

scheduled

to review as-left torque switch settings

on safety-related

non

GL 89-10 valves

and verify that they are the

same

as the as-found settings.

These matters

are scheduled

to be completed

by March 31,

1996.

The inspectors

have concluded that licensee corrective actions for this matter are

acceptable.

2'.6

FIRE

PROTECTION PROGRAM'QUIPMENT INOPERABLE WITHOUT COMPENSATORY

ACTIONS

During this report period,

two instances

were noted in which equipment

required to be operable

by the fire protection

program was inoperable

and

compensatory

actions

were not taken.

The first example involved an improper

clearance

which rendered

reactor building fire protection preaction sprinkler

valve 3-FSV-026-0077

inoperable.

The other issue

was

an inoperable battery

charger switch which had not been promptly recognized

as Appendix

R equipment.

On November 23, at about ll:30 a.m.,

a fire alarm actuated

from the

565'levation

in Unit 3 reactor building.

The alarm was caused

by increased

temperatures

of recently applied paint on

some piping near

a smoke detector.

The reactor building fire protection preaction valve did not function to

charge

the sprinkler lines.

The cause

was traced to the valve "magnetic bypass"

valve not receiving

power

because

a knife switch had

been

opened

between

the valve and the power supply.

The knife switch had

been

opened

as part of a clearance

for other fire

protection work. It had not been recognized that this rendered

the preaction

valve inoperable

and thus compensatory

actions

were not initiated.

On November 24,

one of the inspectors

met with fire protection

manager

and

discussed

the incident.

The inspector verified that immediate corrective

actions,

including surveillance testing to verify operability of the preaction

valves

(HPCI and

RB) had

been performed.

The condition had

been quickly

recognized

by fire protection personnel

who responded

to the alarm.

Those

personnel

were knowledgeabl'e

and if required,

could have tripped the preaction

valve.

The work activity being performed

was demolition/removal of abandoned, fire

protection equipment.

The specific task was being performed

under stage

9 of

DCN 20511

(removal of cables).

The requestor of the clearance

(modifications

worker) for the work included

a circuit to be de-energized

which removed

power

4

0

10

from the preaction

bypass

valve.

(Requestor fills out list of circuits on

SSP-134

form).

The inspectors

met with the leader of the incident investigation

and also

reviewed the completed report.

The inspectors

noted that the investigation

was thorough in regard to review of specific process deficiencies.

Information indicates that the requestor

did not use

a schematic

drawing and

instead,

referred only to connection

diagrams.

Thus the requestor.

failed to

recognize that the switch provided power to the preaction valve.

The

inspector

noted that it was difficult to determine all the loads

on the

subject cable

from the referenced

drawings.

The complexity of'he work plans

contributed to the initial error.

The investigation

concluded that clearance

reviewer had not diligently fulfilled'their responsibilities.

From their reviews,

the inspectors

concurred that the deficiencies

involved;

1) personnel

errors during the development of the clearance

and 2) less

than

thorough reviews of the, clearance.

The inspectors

noted

some similarities

between this incident

and

one involving the Wide Range

Gaseous

Effluent

Radiation Monitor in 1994.

The licensee's

review of the current deficiency

also noted the effluent monitor example in review of previous events.

Although the licensee's

review of the incident was thorough,

the inoperable

fire .protection valve was identified only after it failed to respond to an

actuation.

Previous

examples of clearance

problems

have

been identified.

Information indicates that the valve was inoperable for over.

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

The

inoperable

valve is one example of a violation of the license condition

regarding the-fire protection program.

In late October,

1995, during the performance of the diesel

generator

load

acceptance

testing being performed in preparation for the return of Uni.t 3 to

service,

a test deficiency was generated

when the battery charger

3 power

switch did not properly operate

and provide power to the charger

when placed

in the emergency position.

On December

7,

1995, during the repair of the

battery charger

power switch, personnel

noted that the switch had not been

properly wired and would not operate

in the emergency position.

At this time

it was also recognized that the switch had

an Appendix

R safe

shutd

wn

function to bypass

the load shed logic and provide power to the battery

"

charger in the event of an Appendix

R fire.

PER

BFPER951845

was initiated to

document this condition.

The switch,was properly wired the next day.

Al.though the cause of the wiring error is still being investigated,

the

licensee

has initially concluded that wiring .error may have

been in existence

since the recovery

from the

1975 fire event.

Upon receipt of the

PER, the inspector's

review of the issue indicated that

licensee's

corrective actions

focused

on the wiring error rather than the fact

that appropriate

Appendix

R compensatory

actions

were not taken in response

to

the switch not being functional at least since October

1995.

Section III of

the Appendix

R Shutdown

Program requires, if battery charger

3 is unable to

perform its function, that

a fire watch must

be established if the equipment

is not restored

in seven

days or equivalent

shutdown capability is provided.

The licensee failed to recognize

the Appendix

R function of the switch and did

not take appropriate

compensatory

actions.

The failure to perform these

I~

compensatory

actions is the second

example of a violation of the license

condition regarding the fire protection program.

These deficiencies

are identified as Violation 296/95-64-01,

Fire Protection

Program

Equipment Inoperable Without Compensatory

Actions.

2.7

BIOLOGICAL SHIELD'LOCK REMOVAL FOR REFUELING OUTAGES

The inspector

reviewed the licensee's

actions concerning

the removal of

biological shield. blocks with the reactor at power.

The shield blocks consist

of two sets of blocks stacked

one

on the other

and are located

above the

drywell.

They are accessible

from the refueling floor where they can

be moved

by the overhead

crane in preparation for reactor refueling.

The licensee's

procedure for reactor disassembly

allows removal of the top layer of blocks

while the unit is at

some low power condition progressing

toward the Refuel

mode.

However,

permission

from the refuel floor SRO and Radiological Controls

manager is required if the

mode switch is not in the Refuel or Shutdown

position.

Radiation surveys

are performed during the evolution.

An

engineering

review previously performed

by the licensee

concluded that one

layer of blocks was all that was necessary

for missile protection,

as stated

in the

FSAR, section 5.2.4.6.

2.8

INATTENTIVE FIRE WATCH

On December

21, during

a routine inspection of the Unit 3 Reactor Building, an

inspector

noted that welding work per

WO 95-10970-00 - replacement

of 8 inch

FP piping was being performed.

Although an extinguisher

was in the

immediate vicinity of the job, the fire watch for the job could not be

immediately located

by the inspector.

The job welder

and foreman pointed out

an individual who they thought was the watch;

however,

the individual, when

questioned

by the inspector

proved not to be the assigned fire watch.

After

asking others,

the inspector

found the assigned fire watch talking to

personnel

in a group located

near the south

end of the east

side

CRD

HCU area,

approximately

60 ft from the job area.

The fire watch

had his back turned

toward the hot work area

and was inattentive to the welding being performed.

This issue

was

immediately reported to the

SOS.

BFPER 951902

was initiated

and

a licensee

follow-up was performed

by operations

and maintenance.

Step 5.2.A. I of BFNP Fire Protection

Report

(FPR),

Volume 2, Section I-L,

"Fire Watch Duties

and Responsibilities",

states

that "the fire watch shall

be

on continuous alert for fire, signs of fire and/or

any act that might result

in fire".

Failure of the assigned fire watch to maintain complete control of

his duties

as presented

in the

above

FPR, constituted

a violation of BFNP

procedural

requirements.

However,

the violation will not be subject to

further enforcement

action because

immediate

and effective licensee corrective

actions

were implemented

and the issue. was of minor significance.

This

failure constitutes

a violation of minor significance

and is being treated

as

a non-cited violation, consistent with Section

IV of the

NRC Enforcement

Policy.

This non-cited violation

(NCV) is identified as

NCV 50-296/95-64-04,

Inattentive Fire Watch.

One violation and

two non-cited violations were identified.

0

4

ik

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12

3.0

MAINTENANCE (62703,

92902,

61726,

92901,

37551,

92903)

3. 1

MAINTENANCE AND SURVEILLANCE OBSERVATIONS

Maintenance activities were observed

and/or reviewed during the reporting

period to verify that work was performed

by qualified personnel

and that

approved

procedures

in use adequately

described

work that was not within the

skill of the trade.

Activities, procedures,

and work requests

were examined

to verify proper authorization to begin work, provisions for fire hazards,

cleanliness,

exposure control, proper return of equipment to service,

and that

limiting conditions for operation

were met.

Surveillance tests

were reviewed

by the inspectors

to verify procedural

and

performance

adequacy.

Testing

was witnessed

to ensure that approved

procedures

were used,

test

equipment

was calibrated,

prerequisites

were met,

test results

were acceptable,

and system restoration

was completed.

The following maintenance

and surveillance activities were reviewed

and

witnessed

in whole or in part:

WO 95-22154-00

HPCI Turbine Exhaust Drain Pot Level Switches

On November 28,

1995,

the inspector witnessed

maintenance

personnel

perform

troubleshooting activities

on the Unit 3 HPCI turbine exhaust drain pot level

switches.

The annunciator for this condition was frequently alarming in the

control

room indicating

a high level in the drain pot.

The system design is

such that drain valves automatically

open to control level

when the

appropriate

level switch is actuated.

If the level continues to increase

an

annunciator in the main control

room alarms.

The switch controlling the

operation of the drain valves is BFN-3-LS-073-0008B while the switch actuating

the annunciator is BFN-3-LS-073-0008A.

Maintenance

personnel

found that

switch BFN-3-LS-073-0008A was out of calibration low and in fact was set to

actuate prior to the drain valves opening.

The switch was recalibrated

to the

proper setpoint.

BFPER951799

was initiated to determine

why the switch

setpoint

was incorrect.

The inspector

reviewed the work order

and witnessed

the activity.

The procedures

were adhered to, radiological controls were

adequate,

and the personnel

involved were knowledgeable

concerning this

activity.

The inspector

noted

no discrepancies

with this activity.

WO 95-.23065-00

Solenoid Valve Replacement

For Unit 2 Reactor

Zone Inboard

Exhaust

Damper 2-FCO-64-42

On December

1,

1995 the inspector

observed

the replacement

of this solenoid

following its failure to operate

on the previous day.

The inspector

reviewed

the work order

and noted that

a torque verification for the core plugnut had

not been

signed

by

a

gC representative

as required.

The

gC representative

was

at the job site

and

when questioned

stated that

he had

made the verification

but had simply failed to sign the procedure.

He signed the procedure

at that

time.

The inspector

noted

a high degree of attention

being afforded this

activity.

The activity was performed satisfactorily

and the solenoid

successfully

operated

at the conclusion of the work.

The inspector

noted

no

significant deficiencies with this activity.

)I

~

I

~

13

WO 95-09025-00

Unit 2 RCIC Turbine Exhaust

Line Snubber Rebuild

On Dec m"or 12 the inspector

observed

the disassembly

an" rebuild of RCIC

snubber

BFN-2-SNUB-071-5007.

The inspector noted that the maintenance

personnel

did not use the procedure while performing the work.

The procedure

for this activity was

HPI-O-OOO-SNB002, Hydraulic Shock And Sway Arrestor

Bergen-Patterson

Unit Disassembly

And Reassembly,

and's

a '"Reference

Use"

procedure.

This allows maintenance

to reference

the procedure

as

needed

rather than performing it in a step

by step

manner.

The inspector

noted that

those

personnel

performing the work were extremely knowledgeable

and

experienced

in performing this activity.

The material condition of the area

was well maintained during this activity to avoid contamination of the parts

and snubber internals.

The parts

used

were verified to be in good condition

and appropriate for the job.

The inspector noted that the torque values

used

were obtained

from a,procedure

page attached

to the wall in the room in which

the work was taking place rather than from the page in the procedure that was

included in the work package.

The revision of the page attached to the wall

was revision one while the revision of the procedure

in the .work package

was

revision two.

The inspector

compared

the two pages

and noted that they were

identical.

This was later discussed

with the maintenance

personnel

who stated

that the page attached

to the wall would be removed.

On December

13, while

reviewing the procedure

the inspector noted that precaution

3. 1.2 of this

procedure

stated that if thread lubricant was

used the torque values

were to

be determined

by multiplying the selected

value from the procedure

by 0.90

as

specified in HSI-0-000-PR0017.

Thread lubricant was used during this

activity; however,

the torque values

were not reduced

as described

by the

precaution.

Haintenance

personnel initially agreed that the wrong torque

values

had

been

used

and stated that the snubber

would be loosened

and

retightened

to the

new values.

However,

maintenance later determined that

HSI-0-000-PR0017

stated that if vendor supplied torque values

were available

they should

be used.

Maintenance

stated that the values located in HPI-0-000-

SNB002 were those

recommended

by the vendor

and therefore did not need to be

reduced

as described

in the precaution.

However, discussions

with design

engineering

personnel

indicated that this information may not be completely

accurate.

At the conclusion of the report .period questions still existed

concerning

torque values.

Pending, resolution of this issue, this item will be,

tracked

as Inspector Followup Item 260, 296/95-64-11,

Thread Lubricant Effects

On Torque Values.

TI-137 Core

Power Distribution

During the Unit 3 startup,

O-TI-137, Core

Power Distribution, section 7.5,

Gross

TIP Symmetry Check

and TIP Hookup Verification, the licensee

determined

that TIP channels

A5 and A6,

AB and A9,

and

D6 and

D7 were'swapped.

One of

the purposes for performing this TI was to verify proper hookup of the

individual TIP tubes

and is usually performed following an outage or work

requiring TIP tubing to be removed.

Appendix

4 of the

same procedure

provided

guidance to correct the problem by altering the computer software.

The

licensee initiated

a work order to disconnect

and realign the tubes

when the

drywell can

be accessed.

0

I-0

0

~

~

.

14

The l.icensee

has not yet determined

how the tubes

were misaligned

but

preliminarily stated that it appears

there

may have- been

a problem with

'iabelling.

To conclusively determine

the cause will require

a drywell entry.

BFPER951816

was initiated to determine

the root cause

and develop corrective

action.

The .inspectors

reviewed the process of revising the computer software

,to correct the problem

and concluded this method to be satisfactory,.

3.2

IMPROPER ACTIONS ASSOCIATED WITH FREEZE

SEAL't

2:05 p.m.,

on November 27, during control rod scram time testing,

an

unexpected

decrease

in

CRD system pressure

was noted.

The pressure

decrease

occurred

when

a freeze

seal

plug was thawed before the associated

clearance

boundaries

had been properly restored.

A freeze seal,had

been installed to

perform maintenance

on

a

CRD hydraulic control unit charging line isolation

valve ("588" valve).

The clearance

established

for the work required the

accumulator drain valve (downstream of the freeze plug) to be open.

When the

plug was thawed,

CRD pressure

was ported through the open valve and

a small

spill occurred.

Haintenance

workers shut the valve and stopped

the leakage.

The incident was clearly noted in the operating logs.

The

NRC shift inspector

observed

the incident in the control

room.

On the morning of November 28,

one

of the inspectors

questioned

operators

and the acting operations

superintendent

about

a

PER on the issue.

At that time there

was not

a

PER.

BFPER 951793

was initiated on November

28 to address

the issue.

I

The inspectors

interviewed several

maintenance

personnel

involved in the work

and reviewed'he

work package.

Inspectors

concluded that the incident was

caused

by poor communications

between

operations/maintenance

and

maintenance

not,rigidly following the "freeze seal" procedure

step-by-step:

Maintenance

workers called the

CR and, stated that they were "getting off

the clearance"

and thawing the plug.

Maintenance did not ask for

permission to thaw the plug which was at the time acting

as

a boundary.

NRC inspectors

noted that Step 7. 15 of MSI-0-000-PLGOOI: Installation of

Freeze

Seals,

states:

"Close drain line (if available

and with

Operations

permission)

of secti'on of pipe frozen".

The next step is to

close the refrigerant supply valve.

The drain valve was .tagged

open

on

the clearance

so the maintenance

workers could not operate

the valve.

The drain valve was not shut before the plug was thawed.

The problem with the "588" valve was that it had failed most likely due to

inter-granular stress

corrosion cracking. of the valve wedge ears

as described

in

GE SIL 419.

This causes

the wedges to separate

from the stem.

The

corrective actions

are to replace

the solid wedge with flexible wedges of

different material.

There are

seven

manual isolation valves

on each

HCU

(normally open,

shut only for .maintenance)

which are susceptible

to this.

The

SIL focuses

on three of the valves which if fail could impair a scram

(scram

inlet/outlet

and

SDV lines).

The,inspectors

had previously verified that the

licensee

had refurbished

the three valves

on each

HCU which are highlighted in

the SIL prior to,Unit 3 restart.

The remaining susceptible

valves

are being

replaced

as failures are identified.

The failure of the charging isolation

valves

does not prevent the ability to scram the rod.

lh

IO

15

The inspectors

regarded

the work practice

issues

that led to the freeze

seal

failure as deficiencies.

Performance of the procedural

steps

in order or

better coordination witn operations

would have prevented

the problem.

The

potential safety significance of the freeze

seal failure was that if personnel

did not isolate the flowpath, the ability to move rods with the normal drive

system would be lost due to loss of CRD charging pressure.

The'bility to

scram rods

(even the

HCU being worked) would not be lost since reactor

pressure

would still drive the rod in on

a scram.

PER 951793

was reviewed

by the

HRC on November 29,

1995.

A human performance

evaluation of the incident was directed.

At the close of this inspection

report period, licensee

management

was evaluating

methods of stricter controls

involving freeze seals.

This l,icensee-identified

and corrected violation is being treated

as

a Non-

'Cited Violation, consistent with Section VII.B.l. of the

NRC Enforcement

Pol.icy.

This issue is addressed

as

NCV 296/95-64-02,

Deficiencies

Involvi'ng

Control of Freeze

Seal.

3.3

E(UIPHENT RETURNED TO SERVICE WITHOUT POST

MAINTENANCE TESTING COMPLETED

On December

4,

1995, during control rod exercise testing, control rod 42-39

moved in three notches

(position

48 to position 42) rather than

a single notch

as expected.

Operations

promptly notified reactor engineering

and Technical

Support.

One of the

NRC inspectors

observed

adjustment of the rod speed

which

was performed in accordance

with OI-85.

The inspector noted'hat

the locknut

on the adjustment

device

was found snug.

PER 951815

was initiated to address

the cause of the incorrect

speed.

Subsequently, it was determined that the

insert directional control valve had

been replaced

on

HCU 42-39

on November 8.

Functional testing (verification/adjustment of insert/withdraw times)

was not

performed.

WO 95-20876-00

was used to replace

the directional control valve and it

listed,

as required

PMT, functional testing

.in accordance

with HCI-0-085-

HCU001

and OI-85.

However, the testing

was not performed.

Maintenance

personnel

signed

a step

on November

9 in HCI-0-085-HCUOOI which indicated that

Operations

(a Shift Support Supervisor

instead of SOS/ASOS)

had'een

informed

that the applicable functional test should

be performed.

The

WO was signed

as

PHT complete .at 5:30

pm on November

18 by another Shi'ft Support Supervisor.

There

was not

a signature

from Operations

as the responsible

section

indicating that functional, testing

was completed.

The rod had

been inserted

on the planned

manual scram

on November 9, which

demonstrated

that the rod could perform its safety function.

At the

same time that the rod 42-39 issue

was being investigated,

maintenance

management

al'so

was reviewing other potential

problems with Work Order

processing

and

PHT status.

On December

6,

1995,

PER 951842

was initiated to

address

four mechanical'maintenance

work orders which had

been incorrectly

classified prior to all required

PHT being completed.

This practice

was not

in accordance

with SSP.-6.2,

Maintenance

Management

System.

The work orders

involved maintenance

activities, on several

HPCI and

RCIC valves.

Review of

16

other work orders indicated that the deficient practices

were limited to these

Four examples.

Haintenance

and Operations

management

issued

a memorandum

on December

7, which

clearly stated

expectations

regarding

WO processing

and controls

on

PHT

status.

Operations

and Haintenance

personnel

were briefed

on the guidance.

Emphasis

was placed

on Operations

personnel

verifying that all

PHT was

completed prior to

a system being .declared

operable.

The

PER contained

evaluations

which concluded that although not all the required

PHT was

completed,

equivalent testing which had

been

performed provided assurance

that

the important valves could meet their safety functions

and the systems

were

operable.

The inspector

reviewed the evaluations

and concluded that

operability of the equipment

was adequately

supported.

The inspectors

concluded that appropriate

actions

were taken in response

to

the identified deficiencies

and that management

and operations

personnel

had

been proactive

on the matter.

The safety significance of the specific issues

was limited, however, deficiencies

in such

a fundamental

process

(ensuring

that

PHT is completed prior to return to service)

are of concern.

This

licensee-identified

and corrected violation is being treated

as

a Non-Cited

Violation, consistent with Section VII.B.1 of the

NRC Enforcement

Poli'cy.

This issue is .addressed

as

NCV 296/95-64-03,

Equipment Returned to Service

Without Proper

PHT Completion.

3.4

REVIEW OF 4160

VAC BREAKERS HAINTENANCE ACTIVITIES

On June

15,

1995,

a loss of the

161 Athens line occurred

(IR 95-38;

Paragraph

5.c.) resulting in the loss of the IA & 2A Start Busses.

During recovery

operations,

the

3A CRD pump failed to start

because

the

pump breaker's

"latch

monitoring switch" open circuited.

This in turn, would not allow the charging

motor to charge.

The problem was attributed to

a closing coil plunger being

lodged in place

due .to corrosion

on the plunger shaft.

As

a result of this

problem, periodically, during the last three inspection periods,

an inspector

reviewed past work orders

(WOs) of maintenance

performed

on various Unit 3

4160

VAC Safety-Related

breakers

and observed

the following:

Since

1992, periodic maintenance

(PM) has

been

performed

on all safety-

related

pump breakers

i'.e.,

CS pumps,

RHR p'umps,

SW pumps, etc...

Breakers

are placed

on

a 5-year

PH program and,the

program includes

slide point lubrication

and replacement

of coils if any sticking or

binding,is noted.

The inspector

found that since

1989, only four (4) similar sticking or

binding "latch monitoring switch" problems

have occurred in this type of

breaker

the

"GE AHH 4.16-250 Horizontal" breaker.

Host "sticking"

occurred

due to "dirty" rather than "corroded" plunger shafts.

Since

1990,

PHs

have also

been

performed

on associated

4160

VAC safety-

related

HOV actuator breakers.

On

a continuing 5-year cycle breaker

PHs

are currently being performed'.

3a

Ik

17

All associated

Emergency Diesel Generator/Essential

Buss tie-breakers

have

undergone

comparable

breaker

PHs

and none of the

EDG breakers

have

experienced'imilar

"latch monitoring switch" problems.

After the above review, the inspector concluded that the current licensee

4160

VAC breaker

PH program for safety-related

equipment

was satisfactory.

3.5

OPEN

ITEHS REVIEW

3.5. 1 (Closed)

IFI 50-260/95-56-02,

Use of Nickel-Based

Thread Lubricant on

Gaskets

in TVA Class

"B" Fluid Systems.

In IR 50-260/95-56,

Paragraph

3.2,

an inspector

noted that in August,

1995,

BFNP gA personnel

observed

pipe flange gaskets

being coated with a nickel-

based lubricant; i.e. Nuclear-Grade

"Never-Seez".

The inspector also noted

that

such action could potentially allow this thread lubricant to be in direct

contact with the unit's condensate

system since leeching of this lubricant

into the system

was probable.

During the reporting period,

the inspector

contacted

the thread lubricant vendor

and received confirmation,

both verbally

and in the .form of a vendor specification report, that the lubricant was safe

for such application

and any leeching of this lubricant into the condensate

system

was minimal.

Licensee

personnel

presented

event specifics

and adequate

proposed corrective actions in Plant Problem Evaluation Report

(PER)

BFPER951122.

Based

upon the above,

the inspector's

specific review of vendor

material

and the review of licensee corrective action adequacy,

IFI 50-260/95-

56-02,

Use of Nickel-Based

Thread Lubricant on Gaskets

in TVA Class

"B" Fluid

Systems,

is closed.

Two non-cited violations

and

one inspector followup item were identified.

4. 0

ENGINEERING

4. 1

Secondary

Containment Ventilation Damper Failures

During this report period, the licensee

experienced

several

secondary

containment isolation damper failures

due to sticking solenoid valves.

Prior

to this report period, the licensee

experienced

similar failures in November,

1992 when two Unit 3 dampers failed to close.

The problem was believed to

have

been

caused

by excessive

wear

on the upper disc stem/seat

area

due to

possible chattering

caused

by low power supply voltage or foreign particle

intrusion.

The licensee

examined

the air supply quality and the power

supplies to the solenoids

but determined that both were acceptable.

At that

time other plants in the industry experiencing

solenoid failures postulated

that sticking was at the core-plugnut interface

(CPI)

and was caused

by

lubricant used

by the vendor during assembly.

Based

on this information the

licensee

replaced all the secondary

containment

damper solenoids with

solenoids

containing no,lubricant.

On October 4,

1995,

two secondary

containment isolation dampers,

Unit 2

reactor

zone dampers

13

and

14, failed to isolate

as required.

On October

5

a

third damper,

Unit

1 reactor

zone

damper

14, failed to isolate.

The cause

was

determined

to be due to

a sticking solenoid valve

as previously discussed

in

<5

4N

~

~

~

18

IR 95-56.

In these

cases

when the solenoids

were lightly tapped the damper

repositioned

appropriately.

It was concluded that the solenoid core

was

sticking in the coil.

Following these failures, the licensee

took one of the

solenoids to the vendor for disassembly

and examination.

A black substance

was discovered

on the

CPI which was thought to be the cause of the sticking.

The black substance

was sent to the

TVA central

lab for analysis;

however, it

was determined that the sample size

was too small to make

a positive

identification of the substance.

The remaining two valves were also sent to

the vendor for testing.

The vendor energized

one of the valves for twenty-

four hours at high voltage.

At the end of the period the valve was

deenergized

and the core stuck.

When the solenoid

was lightly tapped

the core

came free.

As follow up, the internal'alve

components

were disconnected

from

the core

and again it was energized.

This allowed the core to be free to move

only by magnetic force from the energized coil or by gravity.

After being

.

energized for one week the valve was deenergized

and again the core stuck at

the CPI.

The inspection also identified that lubricant

had

been

used during

assembly

although the valves were ordered without it.

On November

20 Unit 2

reactor

zone damper

43 failed to close,

however,

the failure was attributed to

faulty limit switches.

On December

11 Unit

1 refuel

zone damper

5 took

approximately

one minute to close instead of the normal five to ten seconds.

No problems

were found with the damper nor was the solenoid confirmed to be

sticking.

The licensee

did not initially consider this

a damper failure.

On

December

13, Unit 2 reactor

zone

damper

42 failed to close.

The cause

was

determined to be due to

a sticking solenoid.

Following this failure, the

resident

inspectors

held discussions

with the licensee. to determine the course

of action being taken

due to the increased failure rate,

the possibility of

common cause failure,

and the operability of the remaining isolation dampers.

Although the licensee

was actively pursuing

a long term solution to this

problem at that time, the short term concern of ensuring operability was not

aggressively

being pursued.

The licensee's

operability evaluation relied

on

weekly cycling of the dampers

which information indicated

was not adequate

to

ensure operability.

The licensee

stated that the failures which had occurred

were from solenoids

whose service life was between thirteen

and seventeen

months.

They indicated that all the solenoids with service lives greater

than

twelve months would be replaced.

By December

17 all the Unit 2 and Unit 3

reactor

zone solenoids

had been replaced.

The licensee

intends to replace

one

solenoid in each pair of the remaining ventilation paths

as replacements

become available

from the vendor.

On December

19, the inspectors

again

met with the licensee to discuss

the

solenoid failures.

The licensee

presented

their. conclusions

concerning

the

failures

and actions

taken or being taken

as

a result.

Results of their

investigation indicate that the solenoid is sticking at the CPI due to the

residue

found at that location.

The vendor

and the licensee

have yet to

conclusively determine the source of the residue.

The licensee

stated that

the

AC coil construction

and high temperatures

associated

with this .model

solenoid contributed to this adhesion

and subsequent

core sticking.

Data also

indicated that the sticking problem does not develop until after approximately

twelve months of operations

The licensee's

short term resolutions

include

replacement

of the existing solenoids

as previously discussed.

Longer term

resolution includes replacing the solenoids with solenoids of a different

design.

The licensee

stated that the

new design

operates

at

a much lower

.

4

~

~

~

19:

wattage

and

CPI temperature

making it less susceptible

to developing core

sticking conditions.

At the conclusion of this report period, the inspector reviewed

NRC

Information Notice 95-53 which discusses

failures of solenoids

due to sticking

at the CPI.

This notice discusses

the possibil,ity of the sticking being due

to the combination of 1'ubricant

used

by the vendor

and thread sealant

used

by

the licensee.

The inspector will continue to monitor the progress, of this

issue

and follow up with the licensee

concerning. this Information Notice.

This issue is identified as Inspector Followup Item 260,296/95-64-10,

Secondary

Containment Ventilation Damper Failures.

4.2

NARROW RANGE TORUS

WATER LEVEL NOT MAINTAINED WITHIN TS LIMITS

On November

15,

1995, while performing

a review of the torus water level

limits for the

BFN Improved Standard

Technical Specifications,

TVA personnel

determined that

a +2 inch offset had

been introduced into the setpoint

calculation for the torus narrow range level instrumentation.

The offset had

been placed into the calculation in 1989 due to the close proximity of the

lower level analytical limit to the technical

specification value.

The

introduction of this offset caused

the level instrumentation

to display

a

value

2 inches less

than actual water level

and ultimately resulted

in Unit 2

violating the upper technical specification limit of -1 inch.

Browns Ferry

technical

specifications

require torus water level to be maintained within a

band o'f -1 inches to -6.25 inches

(instrument "0" corresponds

to elevation

536

feet

8 inches or 15 feet

5 inches of water in the torus).

The licensee

performed

a limited review of past water levels of the Unit 2 torus

and

determined that during the period between

October 8-14,

1995, the water level

within the torus exceeded

the technical specification limit by approximately

one inch.

No further review of past Unit 2 records

was conducted

as

TVAs

engineering

analysis

indicated that

no detrimental effects

on long term torus

integrity would occur if indicated torus level did not exceed

Technical

Specification value.

This matter

was reported to the

NRC in accordance

with

10 CFR 50.73(a)(2)(i)(B) in an

LER dated

December

14,

1995.

The licensee's

immediate corrective actions for this matter were to place

a

more restrictive administrative

band

on the torus water of -3 inches to -5.5

inches to negate

the

2 inch offset for both Units

2 and

3 (at the time of

discovery, Unit 2 was operating at

100 percent

power and Unit 3 was in cold

shutdown preparing for restart following the

10 year outage).

Prior to the

startup of Unit 3, the torus narrow range instrumentation

was recalibrated

to

remove the

2 inch offset.

The offset was subsequently

removed

from the Unit 2

instrumentation

and the licensee

returned to their normal administrative

band

of -2 inches to -5.5 inches.

During 'the inspector's

review,

a number of questions

arose related to this

matter.

The first question deals with the instrument

accuracy of the torus

water level narrow range instrumentation.

The licensee's

setpoint

documentation for this instrumentation

states

that the accuracy

range is +/-

1.75 inches.

The inspector.

questioned,

when applying this accuracy

range to

the licensee's

administrative level limits of -2 inches to -5.5 inches,

how it

can

be assured

that the

TS limits are not exceeded.

Discussions

held with NRR

0

20

personnel

indicated that the licensee's

practice of utilizing the analytical

limit to bound instrument error is acceptable

for TS indication

instrumentation.

A second

question related to thi's matter

.'".mls with the

potential, that the licensee

exceeded their design analytical limit of +1 inch

when the

2 inch offset was present

in the setpoint.

The inspectors

brought

this matter to the attention of the licensee's

engineering

department

who in

turn contacted

the .NSSS vendor

(General 'Electric).

GE informed the licensee

that additional

margin existed

above. the

+1 inch upper analytical limit and

the appropriate

supporting documentation

would be provided.

As mentioned previously, the

2 inch offset resulted

in the licensee

exceeding

the Unit.2 torus

TS limit of -1 inch.

A'fter a detailed review of this matter,

the inspectors

concluded that this issue constitutes

a violation of minor

significance

and is being treated

as

a 'Non-Cited Violation, consistent with

Section

IV of the

NRC Enforcement Policy.

This issue is identified as

NCV

260/95-64-09,

Violation of Torus Water Level TS.

4.3

REACTOR RECIRCULATION PUMP SEAL PURGE

EFFECTS

ON THE NUCLEAR HEAT

BALANCE CALCULATION

While investigating industry events

the licensee

determined that

a small

amount of control rod drive flow used for reactor recirculation

pump seal

purge

was not accounted for in the calculations of the nuclear heat balance.

Although not considered

to significantly affect the results of the core

thermal

power calculation,

BFPER951879

was initiated to document the concern

and ensure

the calculation

was reperformed.

The Operations

superintendent

issued'n

Operations

Daily Instruction directing that power be limited to 3292

Mwt rather than rated

power of 3293

Mwt until this was completed.

The amount

of flow into the reactor which was unaccounted

for was approximately 2-3 gpm.

The licensee

determined that the error in the reactor thermal

power caused

by

this flow was approximately 0. 1 to 0.5 Mwt.

Engineering

concluded that

conservatism

and component

inaccuracies

already factored into the calculation

would compensate

for this error and therefore this additional flow did not

result in reactor

power exceeding

the licensed limit of 3293 Mwt.

After

engineering

determined that the error was negligible the daily instruction

limiting power was rescinded.

The licensee will continue to follow this issue

both with the industry groups

and the vendor.

One Inspector

Followup Item and

one Non-cited Violation were identified.

5.0

PLANT SUPPORT

The inspectors

toured the protected

area

and noted that the perimeter

fence

was intact

and not compromised

by erosion

or, disrepair.

The fence fabric was

verified to be intact and secured.

The inspectors

observed

personnel

and

packages

entering the protected

area

and verifi'ed they were searched

either by

special

purpose detectors

or physical

patdown.

Improvement

was specifically

noted regarding

the access

control problems discussed

in IR 95-60.

No violations or deviations

were identified.

0

hi

0

~

~

21

6.0

REVIEW OF

NRC ORAT INSPECTION FINDINGS

The ir~; ctors reviewed the findings described

th

Unit 3

ORAT Inspection

Report (95-201).

Several

deficiencies

and open items were identified.

6. 1

DEFICIENCY 50-296/95-201-05,

PROCEDURES

AND TRAINING WERE

NOT ADEQUATE

TO

ENSURE FIRE DANPERS

WOULD CLOSE

IN A FIRE AREA

The

ORAT identified that the procedural link which guided operators

to the

procedures

to secure/isolate

ventilation systems

in case of a fire was weak.

Paragraph

6. 14 of Inspection

Report 95-60 describes

a detailed resident

inspector review of the licensee's

immediate actions in response

to the

ORAT

finding.

The inspector verified that the licensee

has modified procedures,

enhanced

labeling,

and trained operators.

Additionally, the

summary section

of the

ORAT report stated that the licensee

took prompt and adequate

corrective actions.

The

ORAT report specifically described

EPIP

21

as the deficient procedure.

EPIP

21 is only one, of the procedures

which should

be referenced

in event of a

fire.

Volume

2 of the Fire Protection

Report contains

the detailed Fire "Pre-

Plans" which will be carried to the scene

and

used

by the fire brigade leader.

These pre-plans

contain guidance

in the "special precautions"

section stating

"If zone isolation is required to stop the propagation of smoke, notify the

SOS".

Both the

new procedure

(AOI-26-1) and the old procedure

(AOI-30-1)

state that actions to secure ventilation are to be taken

based

on

recommendation

of the fire brigade leader.

In discussions

with the inspector,

the brigade leaders

indicated that this is practiced

in drills by

recommendations

to the incident

commander

(ASOS).

The inspectors

concluded

that the operators

would refer to the AOI. as necessary if specifical.ly

directed to secure ventilation.

Securing ventilation is

a relatively simple

activity that control

room operators

would most likely be able to perform

without specific procedural

guidance

once directed to do so.

The apparent

discrepancy

is that the Fire Hazards Analysis states

that

procedures

are in place to require the control

room to initiate

HVAC zone

isolation when

a fire is verified in an area.

Additional review of this issue

was conducted.

.In addition to the Fire Protection

Report statements,

the

inspector noted other documents

which indicate that procedures explicitly

direct shutting off ventilation in the event of a fire.

The licensee's

internal

response

to IN 89-52 indicated that AOI-30-1 had

been

issued to

address

the concern

in the IN.

A 1985

INPO document

involved similar fire

damper issues

and was also

addressed

by AOI-30-1.

The inspector also noted

that

CATO 23001-BFN-01

(employee

concern)

addressed

this

same issue.

The

original

CATD corrective action plan required verification that dampers

would

shut against air flow but was later revised

such that it also relied upon AOI-

30-1

as procedural

guidance to isolate ventilation.

The inspector

noted

documentation

indicated that many of the dampers

have

been upgraded/replaced

with dampers that are designed

to shut against air flow (meet

UL 555), but

that the dampers

are not tested

against air flow.

55.

0

22

The inspector

noted that the revised procedure,

like the original AOI, relies

on fire brigade'ecommendations

for ventilation operations.

The inspector

concluded that the pro=edures

do not require implementation of the actions

as

specifically stated

in the Fire Protection

Report statement.

Additional

discussions

were held with the licensee

and the

ORAT inspector

who identified

the issue.

The licensee

indicated that it is not desirable

to always

secure/isolate

ventilation in the event of a fire.

The licensee

stated that

a

50.59 evaluation

would be performed

and the statements

in the Fire Protection

Report will be revised.

The resident

inspectors

requested

that the evaluation

specifically address

the issue of fire dampers

shutting with fans operating.

This issue will'e addressed's

Unresolved

Item 260,296/95-64-08,

Fire Damper

Procedural

Controls,

pending additional

NRC review of the licensee's

actions.

6.2

DEFICIENCY 50-296/95-201-03,

FAILURE TO RECORD

REQUIRED INFORMATION IN

THE CONTROL

ROOM

LOG AS REQUIRED

BY PROCEDURE

The

ORAT identified examples

in which the operators failed to log information

specifically required

by procedures

to be logged.

The resident

inspectors

have noted other isolated

instances

in which log entries should

have

been

more

complete.

Technical Specification 6.8. l.l.a requires that written procedures

recommended

in Appendix A of Regulatory

Guide 1.33,

Revision 2, February

1978,

be

established,

implemented,

and maintained.

Section

1.h of Appendix A in

RG 1.33

recommends

procedures

for log entries.

SSP-12. 1,

"Conduct of

Operations,"

Section 3. 11.3.B states

in part:

"The following information

shall

be recorded

in at least

one station log..."

The specified information

includes

abnormal

plant configurations,

status

changes

to safety-related

and

major plant equipment including the instruction

and section

used,

occurrence

of any reportable

events, initiation and completion of surveillance

instructions (SIs), entering

and exiting Technical Specification

(TS) action

statements,

testing activities including the procedure

number

and problems,

and events.

The listed examples

were clearly examples of issues that the

licensee's

procedures

require to be logged.

It should

be noted that the

operators

sometimes

do not record in the control

room logs all aspects

of

incidents which are recorded

in other documents

such

as

Problem Evaluation

Reports, test deficiencies,

or personnel

statements.

After detailed

review of the examples,

the inspectors

concluded that this

failure to follow procedures

constitutes

a violation of minor significance

and

is being treated

as

a Non-Cited Violation, consistent with Section

IV of the

NRC Enforcement Policy.

This issue is identified as

NCV 296/95-64-07,

Failure

to Record Information in Unit Logs.

6.3

DEFICIENCY 50-296/95-201-01,

SOME OPERATIONS

PROCEDURES

MERE NOT

ADEQUATE.

The

ORAT identified three

examples

in which it appeared

that procedures

were

not appropriate

to the circumstances

in which they were used.

<i

23

Example A:

On October

13,

1995,

Work Order 95-18774-00,

"RPS Troubleshooting

Proposed

Plan of Action" failed to. include provisions to prevent the closure of 3-FCV-

74-67,

RHR LPCI inboard isolation valve,

as

was intended.

Consequently,

residual

heat removal'hutdown cooling was interrupted during the performance

of the work order.

An NCV was issued

in Inspection

Report 95-60

on this incident.

'The licensee

failed to treat the troubleshooting

as

a "high risk activity" as required

by

their procedures.

This failure to fol.low procedure

resulted

in a significant

reduction in the layers of defense

intended to prevent

such

an occurrence.

Personnel

errors during development and'eview of the troubleshooting

work

order caused

the event.

After detailed review of the issue,

the resident

inspectors

concluded that the deficiency was related to the,licensee's

failure

to fol-low established

procedures

in the formulation of:the plan., As stated

in

the

ORAT report,

the safety significance

was limited due to plant conditions

and the issue

was conservatively reported to the

NRC operations

center.

Example

B:

Operating Instruction, 3-0I-73,

"High 'Pressure

Coolant Injection System,"

Revision 0, Illustration 1, failed to provide adequate

instructions to perform

wire lifts on .Panel

3-9-39.

On October

11,

1995, operations

personnel lifted

the wrong wire.

This action resulted

in disabling of the manual trip function

for the high pressure

coolant, injection (HPCI) system

steam, driven turbine.

This deficiency occurred during testing of the

HPCI system

on auxiliary steam

prior to HPCI being declared

operable.

The evolution was being performed

primarily to flush the

HPCI discharge .lines.

One of the resident

inspectors

was observing this testing at the HPCI,turbine .when the deficiency was

identified.

The procedure

included

a confirmation that the turbine could be

tripped.

Immediately after the problem was identified, the testing

was

halted,

and the issue

was addressed.

The inspectors

reviewed

PER 951473.

The problem was that the panel

side wire

was lifted .instead

of. the field side wire.

'OI 73 for both 'Units

2 and

3 have

been revised to more clearl'y reflect the correct "field side" wires to be

lifted.

The inspector

reviewed the procedure

and concluded that it does

provide more clear directions

on which wire to lift.

Operators

have

been

informed on the problems described

in the

PER.

The

PER remains

open pending

additional. review of procedures

for similar.,problems.

The wire lift being performed

was to permit testing of HPCI on low pressure

steam.

'HPCI would be inoperable during such testing.

The OI and the TI both

included specific requirements

to confirm that the

HPCI trip function was

operable prior to running HPCI.

The OI has

been utilized successfully

(Unit

2) in the past to lift the leads for HPCI operations.

The enhancements

to the

procedure

provide better guidance to the operators.

The inspectors

concluded

that this issue

involved

a personnel

error and that the licensee correctly

implemented

procedures

for testing deficiencies

and identification/resolution

$5

l

4

of the problem.

The inspectors

did not identify a violation of regulatory

requirements.

Example

C:

Technical

Instruction, 3-TI-343,

"HPCI Injection Flush," Revision 0, Step

7. 13, states,

"CLOSE HPCI

PUMP CST TEST VALVE, 3-FCV-73-35".

During a test,

the control

room operator throttled the valve to maintain the desired

HPCI

flow rate to the reactor pressure

vessel

to prevent reactor cavity overflow.

This example also involved HPCI testing prior to the system being declared

operable.

As stated

in the

ORAT report, the procedural error had

no safety

significance,

the actual

actions

performed were correct,

and the procedural

problems

were documented

immediately after the test

was run.

After additional

review, the resident

inspectors

concluded that the regulatory concern

was that

administrative

requirements

for revision of procedures

were not followed.

This example will be grouped with the deficiency involving maintenance

procedures

not being followed since that issue involved similar failure to

adhere to procedure

requirements

on procedure

adherence/revisions

(paragraph

6.4).

Available information indicates that in both of these

examples,

the licensee identified the problem and pursued corrective action

independent

of NRC involvement.

This licensee-identified

and corrected

violation is being treated

as

a. Non-Cited Violation, consistent with Section

VII.B.I of the

NRC Enforcement Policy.

The two examples will 'be addressed

as

NCV 296/95-64-06,

Failure to Follow Requirements

for Procedure

Changes.

6.4

DEFICIENCY 50-296/95-201-04,

MAINTENANCE PROCEDURES

WERE NOT FOLLOWED.

The

ORAT report clearly indicates that the issue

involved failure to follow

administrative

procedures

for revision of procedures.

As stated

in the

report,

the work was performed satisfactorily

and the procedure

was

subsequently

revised to reflect the

new acceptance

criteria prior to the

ORAT

inspector's

observation that the procedure

was not followed.

The regulatory

concern is that the procedural

requirements

(follow procedure

or revise it)

were not met.

This example involves

a regulatory concern similar to,that

discussed

above

and will be addressed

as

an example of NCV 296/95-64-06.

6.5

OBSERVATION 50-296/95-201-02,

OPERATIONS

PERSONNEL

FAILED TO

FOLLOW GOOD

OPERATIONS

AND 'RADIOLOGICAL CONTROL PRACTICES

The examples listed in the

ORAT report address

two areas of Operations

performance;

good operations

practices,

and good radiological control

practices.

The inspectors

conducted

additional

inspections

to determine if

the examples

represented

declining or marginal

performance.

For over

10 days

in late November,

NRC inspectors

performed continuous

observations

of Unit 3

control

room activities.

While a few examples of inattention to detail

were

noted

by the inspectors,

there were

no observations

of inappropriate

performance

regarding annunciators.

No additional observations

of weak

radiological

controls practices

by Operations

personnel

have

been

noted

despite

the extensive

inspection activities conducted for the Unit 3 restart.

The resident

inspectors will continue to monitor performance

in these

areas.

<P

~

~

25

6.6

OBSERVATION 50-296/95-201-06,

ENGINEERING TO COMPLETE THE REACTOR VESSEL

HEAD VENT LINE PIPE

WHIP ANALYSIS

One of the resi'dent

inspectors

met with engineering

management

and reviewed

documentation

associated

with this issue.

In response

to the questions

raised

by the

ORAT inspector,

the licensee

provided information which indicated that

the l.ine does not represent

a potential

pipe whip situation in which the

piping could impact the containment spherical

shell

head.

Information was

provided which indicated that the original

GE pipe rupture analysis for BFN

concluded that the

damage potential

from pipe breaks of the size piping

involved does not have

a significant effect.

Additionally, documentation

was

provided which demonstrated

that the jet load effects

on the shell

head

closure

had

been considered

in the shell analysis.

The, resolution

and

evaluation of the

ORAT inspector's

questions

was documented

as attachment VII

of Calculation

CD-93999-950476

Pipe Rupture Evaluation for the

BFNP Unit 3

Restart.

The resident

inspector concluded that the issue

had

been

sufficiently resolved.

One unresolved

item and two non-cited violations were identified.

7.0

EXIT (30703)

The inspection

scope

and findings were summarized

on December

30,

1995,

by L.

Wert with those

persons

indicated

by an asterisk in,paragraph

1.

The

inspectors

described

the areas

inspected

and discussed

in detail the

o

inspection results.

A listing of inspection findings is provided.

Proprietary information is not contained

in this report.

Dissenting

comments

were not received

from the licensee.

Item Number

Status

Descri tion and Reference

VIO 50-296/95-64-01

NCV '50-296/95-64-02

NCV 50-296/95-64-03

NCV 50-296/95-64-04

NCV 50-296/95-64-05

Open

Open

8 Closed

Open

& Closed

Open

& Closed

Open

&

Closed'ire

Protection

Program

Equipment Inoperable Without

Compensatory

Actions

(paragraph

2.6)

Deficiencies Involving Control

of Freeze

Seal

(paragraph

3.2)

Equipment Returned to Service

Without Proper

PHT Completion

(paragraph

3.3)

Inattentive Fire Watch

(paragraph

2.8)

HPCI Flow Controller Switch

Not in AUTO (paragraph '2.3)

Nl

0

NCV 50-296/95-64-06

NCV 50-296/95-64-07

URI 50-260,

296/95-64-08

NCV 50-260/95-64-09

IFI 50-260,

296/95-64-10

IFI 50-260,

296/95-64-11

IFI. 50-260/95-56-02

8.0

ACRONYHS

26

Open

8 Closed

Open

5 Closed

Open

Open

5 Closed

Open

Open

Closed

Failure to Follow Requirements

for Procedure

Changes

(paragraphs

6.3 and 6.4)

Failure to Record Information

in 'Unit Logs (paragraph

6.2)

Fire Damper Procedural

Controls

(paragraph

6. 1)

Violation of Torus Water Level

TS (paragraph

4.2)

Secondary

Containment

Ventilation Damper Failures

(paragraph

4. 1)

Thread Lubricant Effects

On

Torque Values,

(paragraph

3. 1)

Use of Nickel-Based

Thread

Lubricant on Gaskets

in TVA

Class

"B" Fluid,Systems,

(paragraph 3.5.1)

AOI

ASOS

BFN

BFPER

BOP

'CATO

CFR

CPI

CR

CRD

CS

CST

DCN

EDG

EGR

EHC

EMS

EPIP

FP

FPR

FSAR

GE

gpm

HCU

HPCI

Abnormal Operating Instruction

Assistant Shift Operations

Supervisor

Browns Ferry Nuclear Plant

Browns Ferry Problem Evaluation 'Report

Balance of

Plant'orrectiveAction Tracking Document

Code of Federal

Regulations

Core-Plugnut Interface

Control

Room

Control

Rod Drive

Core Spray

Condensate

Storage

Tank

Design

Change Notice

Emergency Diesel

Generator

Electro-Governor

R

Electric Hydraulic Control

Equipment

Hanagement

System

Emergency

Plan Implementing Procedures

Fire Protection

Fire Protection

Report

Final Safety Analysis Report

General

Electric

gallons per minute

Hydraulic Control Unit

High Pressure

Coolant Injection

I

ik

0

27

IFI

IN

INPO

IR

LPCI

LPRH

MOV

HRC

Hwt

NCV

NRC

NRR

OI

ORAT

PER

PH

PHT

gA

gC

RC IC.

RB

RG

RHR

.RPS

SDV

SE

SI

SIL

SPDS

SOS

SRO

SSP

SRV

SW

TI

TIP

TS

TVA

UL

UNID

URI

VAC

VIO

'WO

rations

Team

Inspector Followup Item

Information Notice

Institute for Nuclear

Power

Ope

Inspection

Report

Low Pressure

Coolant Injection

Local

Power

Range Monitor

Motor Operated

Valve

Management

Review Committee

Megawatts-Thermal

Non-cited Violation

Nuclear Regulatory

Commission

Nuclear

Reactor Regulation

Operating Instruction

Operational

Readiness

Assessment

Problem Evaluation Report

Preventive

Maintenance

Post Modification Testing

guality Assurance

guality Control

Reactor

Core Isolation Cooling

Reactor 'Building

Regulatory

Guide

Residual, Heat

Removal

Reactor Protection

System

Scram Discharge

Volume

Safety Evaluation

Surveillance Instruction

Service Information Letter

Safety Parameter

Display, System

Shift Operation Supervisor

Senior Reactor Operator

Site Standard

Practices

Safety Rel:ief Valve

Service

Water

Technical

Instruct'ion

Traversing

Incore Probe

Technical Specifications

Tennessee

Valley Authority

Underwriters Laboratory

Unique Equipment Identification

Unresolved

Item

Volts Alternating Current

Violation

Work Order

~\\

~O