ML18039A348

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Insp Repts 50-259/98-02,50-260/98-02 & 50-296/98-02 on 980301-0411.Violations Noted.Major Areas Inspected: Operations,Engineering,Maint & Plant Support
ML18039A348
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 05/05/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18039A346 List:
References
50-259-98-02, 50-259-98-2, 50-260-98-02, 50-260-98-2, 50-296-98-02, 50-296-98-2, FACA, NUDOCS 9805210295
Download: ML18039A348 (67)


See also: IR 05000259/1998002

Text

U.S.

NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:-

License

Nos:

50-259,

50-260.

50-296

DPR-33,

DPR-52,

DPR-68

Report Nos:

50-259/98-02,

50-260/98-02,

50-296/98-02

Licensee:

Tennessee

Valley Authority

Facility:

Browns Ferry Nuclear Plant, Units 1, 2.

8 3

Location:

Corner of Shaw and Browns Ferry Roads

Athens,,AL

35611

Dates:

March 1,

1998 - April 11,

1998

Inspectors:

L. Wert. Senior Resident

Inspector

J. Starefos,

Resident

Inspector

E. DiPaolo. Resident

Inspector

G. Hopper,

Reactor

Engineer

(Section 05. 1)

C. Smith, Reactor

Inspector (Section El. 1)

W. Smith, Reactor

Engineer

(Section 05. 1)

Approved by:

H. 0. Christensen,

Chief

Reactor Projects

Branch

6

Division of Reactor

Projects

98052i02'P5

980505

PDR

ADGCK 0500025'P

8

PDR

Enclosure

2

EXECUTIVE SUMMARY

Browns Ferry Nuclear

Plant, Units 1. 2.

8 3

NRC Inspection Report 50-259/98-02.

50-260/98-02,

50-296/98-02

This integrated

inspection included aspects of licensee operations,

engineering,

maintenance,

and plant support.

The report covers

a six-week

~

~

er iod of resident inspection

and inspection in the areas of Licensed Operator

raining and Engineering

by a Region II Division of Reactor

Safety Inspector

and two Reactor

Engineers.

~oereti one

Overall conduct of a complex surveillance involving 3EC shutdown board testing

was good.

Self-checking

and communications

practices

were observed to be

strong. 'he Senior Reactor Operator

(SRO) coordinating the testing

was well

prepared

and applied excellent supervisory oversight throughout the test.

The

SRO promptly identified and corrected

two personnel

errors during the testing.

The investigation

and immediate corrective actions for an emergent electrical

board switch problem were performed well (Section 01. 1).

Licensee

management

promptly and aggressively

responded to an

NRC observation

that

an expectation

contained in a standing order for control rod exercise

testing

was not implemented.

The issue

was thoroughly reviewed by the

licensee,

documented in the corrective action program,

and acceptable

corrective actions were completed.

In general.

the inspectors

have noted

increased

Operations

Department sensitivity to meet

management

expectations

during the performance of this testing (Section 01.2).

Control

room operators

properly inserted

a manual scram after entering

Region

1 of the core thermal

power to flow diagram following a recirculation

pump runback.

The runback resulted

when

a breaker

opened in the recirculation

pump control circuitry.

The problem was caused

when an engineer

taking

measurements

in an instrumentation

cabinet allowed

a metal tape measure to

contact a'use

holder.

Operator

response

following the scram was good.

The

peer

check performed

on the shutdown cooling lineup was considered

a good

practice.

The Incident Investigation

was thorough in review of the scram

and

equipment

issues

(Section 01.3).

The inspectors

concluded tha't

a recent increase

in the number of operations

performance

issues

did not constitute

a significant negative trend.

The

safety significance of many of the items was minor and

a low threshold of

problem identification was noted (Section 01.4).

Attendance of support group representatives

(i.e.. fire protection, security.

maintenance,

and engineering)

at the shift turnover

meeting

was considered

a

good practice.

Board walkdowns by operators

were detailed.

thorough.

and

consistent

from crew to crew.

Pre-shift reviews of 'required documentation

were generally thorough (Section 01.5).

The licensed operator requalification program was adequate

with respect to the

examination question sampling process,

remediation training, operating

examination content validity, and feedback of plant events

and incidents into

the training curricula.

However. the written examinations

contained

questions

of marginal discriminatory value,

and therefore.

did not fully meet the

standards

established

in NUREG'-1021.

Interim Revision

8 (Section 05.1).

The licensed operator activation/reactivation

process

was incorrectly

implemented resulting in operator licenses

being certified active when in fact

they were not.

As a result. the licensee failed to meet the minimum shift

crew requirements

on several

occasions.

A violation was identified by the

inspectors for noncompliance with Technical Specification (TS) 6.2.2.a.

(Violation 259,260,296/98-02-01.

Failure to Meet Minimum Shift Crew

Requirements)(Section

05. 1).

In several

observed control

room simulator training scenarios,

the crew

successfully

recognized

the major events'tilized

response

procedures,

and

stabilized the unit.

In general,

operator

performance

issues

such

as

use of

procedures

and communications

were addressed,

however management

expectations

for self-checking were not consistently

emphasized.

During observation of

the critique sessions,

the resident

inspectors

noted several

examples

which

indicated that the training personnel

were not consistently enforcing high

standards

of overall proficiency (Section 05.2).

Maintenance

The licensee did not initially perform an aggressive

review of the inspector's

concern that

SBGT testing relied upon the skill of the maintenance craft to

work around procedural

obstacles.

The

NRC subsequently

identified that the

model of DOP generator

used for testing of the Standby

Gas Treatment

(SBGT)

and Control

Room Emergency Ventilation

(CREV) systems

was not equivalent to

that model required

by the procedure.

A violation was identified for failure

to follow testing procedures.

(Violation 259,260 '96/98-02-02 'ailure to

Follow High Efficiency Particulate Air Filter Testing Procedures).

Additional

NRC review identified that the procedure for testing the

SBGT downstream

filter did not meet the requirements of American National Standard Institute

(ANSI) N510-1975

as required

by TS.

(Violation 259.260.296/98-02-03,

Inadequate

Testing of Downstream Standby

Gas Treatment

HEPA Filter)(Section

Ml.1) .

Periodic replacement of the High Pressure

Coolant Injection System turbine

exhaust

rupture disc assembly

was performed satisfactorily except that the as-

found inspection

process

was not adequate to'identify that the disc material

was degraded.

The licensee did not identify the degradation until the

inspectors

questioned

the inspection

method.

(Violation 260/98-02-04,

Failure

to Identify Degraded

HPCI Rupture Discs)(Section

M1.2).

Overall. conduct of Fix-It-Now team work was good.

The inspectors

questioned

the procedural

guidance

and implementation regarding the use of personnel.

in

some cases,

to ensure that

a component

was maintained in the safe position

instead of using

a clearance.

Licensee

management

is reviewing the practice

to determine if procedural

guidance is appropriate

and management

expectations

were met.

Additional

NRC review of the licensee's

evaluation is necessary.

(Inspection Follow-up Item 260,296/98-02-05.

Use of Personnel

in Place of

Equipment Clearances)(Section

Ml.3).

Major maintenance activities on two residual

heat

removal service water

pumps

were conducted well.

Placement of the

pump assemblies

was performed carefully

and actions to address

shaft wear were good (Section M1.4).

En ineerin

The inspector concluded that the licensee's

gualified,50.59 Preparer Training

met ANSI-3.1-1981 (Section El.l).

Six 10 CFR 50.59 safety evaluations

were chosen for review, five were

determined to be technically adequate.

One safety evaluation

had

a minor

deficiency, in that the

SER incorrectly stated the scope of the change

(Section El. 1) .

Plant

Su

ort

The licensee properly posted required notices to workers

as required by 10 CFR 19. 11.

Technical

Information Center

personnel

were knowledgeable of the

locations of documents

required to be available to workers (Section R1.1).

~RO

Summar

of Plant Status

Unit 1 remained in a long-term lay-up condition with the reactor defueled.

Unit 2 operated at or near full power.

Unit 3 operated at or near full power.

On Harch 27.

1998,

power was reduced

to about

65 percent

rated for flux suppression

testing

and control rod

adjustments.

One additional

rod was inserted to suppress

flux near

a fuel

leak and power was restored to full rated several

days later.

On April 7,

1998, the unit was manually scrammed after the recirculation

pumps

ranback.

The runback resulted

when

a breaker

opened in the recirculation

pump control

circuitry.

The problem was caused

when an engineer

taking measurements

in an

instrumentation

cabinet allowed

a metal tape measure to contact

a fuse holder.

Section 01.3 contains additional details.

While performing the inspections

discussed

in this report, the inspectors

reviewed the applicable portions of the Updated Final Safety Analysis Report

(UFSAR) that related to most of the areas

inspected.

Section Hl. 1 describes

issues

involving testing that was not conducted in the manner described in

Section 5.3 of the

UFSAR.

No other issues

were identified.

~l.

0

Ol

Conduct of Operations

01. 1

4kV Shutdown

Board Undervolta

e Start of Diesel

Generator

Division II

Surveillance Test

and Failure of the

3B 480V Shutdown

Board to Transfer

to Alternate

Su

1

a.

Ins ection

Sco

e

71707

61726

One of the resident inspectors

observed significant portions of 3-SI-

4.9.A.4.b(II), 4kV Shutdown

Board Undervoltage Start of Diesel Generator

Division II.

During the testing,

the 3B 480V Shutdown

Board failed to

transfer to its alternate

supply.

The inspector observed

some of the

troubleshooting activities

and corrective actions.

b. Observations

and Findin s

The inspector

observed the portions of the test associated

with the

3C

4kV Shutdown

Board and the

3EC Emergency

Diesel Generator

(EDG).

Performance of the test

began

on Harch 10,

1998.

The briefing held

prior to testing

was thorough.

All pertinent

items listed in Section

3.6 of Site Standard

Practice

(SSP)-12. 1, Conduct of Operations,

were

addressed.

The Senior Reactor Operator

(SRO) who was the lead performer

of the test led the briefing.

Specific responsibilities

by involved

performers

were discussed.

The

SRO had closely reviewed the test

procedure in preparation for the test.

For example.

steps necessitating

entry into Technical Specification

(TS) Limiting Condition for

Operations

(LCOs) or Appendix

R issues

were marked

as such.

Limitations during alternate

power alignments

were also discussed.

\\

2

The initial portions of the test went well.

Transmission

and

Power

Services

(TPS)

and Operations

personnel

verified correct functioning of

key relays

and alarms.

The inspector observed that the

TPS personnel

consistently utilized good self-checking techniques.

Independent

verification of the removal of test plugs was performed correctly.

Step 7.2.45 required transfer of the

3B 480V Shutdown Board to its

alternate

power source in accordance

with Operating Instruction (OI)-

57B.

A separate

briefing was held before the evolution.

The inspector

noted that notification of other site organizations

was

made before the

transfer.

The inspector

observed

two SROs in the attempt to transfer

the 480V shutdown board.

The operators

were actively referencing the

rocedure

and correctly performed the steps

leading

up to closing the

reaker switches.

The inspector observed that the

SRO fully moved the

control switch handle to the close position.

The alternate

breaker

did

not shut and the

SROs promptly closed the normal breaker

as directed

by

the procedure

and halted the testing evolution.

The failure of the board to transfer resulted in a loss of the 3B

Reactor Protection

System

(RPS) bus.

A 10 CFR 50.72 notification was

made to the

NRC Operations

Center.

The potential

loss of an

RPS bus

had

been addressed

in the briefing.

The inspector

observed that control

room personnel utilized procedures to respond to the engineered

safety

feature system actuations.

Two minor discrepancies

were observed.

The

operators

had to shut off one train of Standby

Gas Treatment to correct

a reactor building static pressure

condition which inhibited restoration

of reactor

and refueling floor ventilation.

This issue

was later

addressed

as

an operator work around.

The Unit Supervisor initially did

not recognize that

a

TS Limiting Conditions for Operation

(LCO) entry

was required

due to the mode switch shutdown

scram function being

inoperable for

a short time after the transfer failed.

Procedure

3-AOI-

-99-1,

Loss of Power to One

RPS Bus,

and

GE Service Information Letter

(SIL) 344 describe

how a relay race

may cause this condition and

how to

clear the condition.

The condition was subsequently'orrected

within

several

minutes in accordance

with procedures.

The licensee

developed

a detailed troubleshooting

plan to systematically

examine the problem.

After some investigation,

technical

support

ersonnel

noted that

a wire connected to the back of the alternate

reaker control switch was very close to a moveable contact finger

and

may have prevented the contacts'from closing as the switch handle

was

rotated to the close position. It was postulated that the slip-on cover

on the back of the

GE SB-1 type switch was pressing the wire down enough

to inhibit contact closure.

On March 12. the licensee

established

proper plant conditions

and attempted transfer of the board again.

The

resident

inspector

observed that the suspect wire was barely clear of

the contact finger before the switch was

moved and appeared

to just

contact the finger as it was operated.

Under the wire there

was

some

marks indicating that the wire had rubbed against the contact in the

past.

When workers

removed the lid or back enclosure

from the switch

cover and installed just the edge piece,

the inspector noted that the

cover edge

was against the wire and just slight pressure

on the piece

was sufficient to press the wire down.

By examining

a similar

uninstalled switch, the inspector

noted that it was easy to hold the

moveable contact

as the control switch handle

was rotated

due to some

"float" or free motion in the switch design.

A Problem Evaluation

Report

(PER)

was initiated to address

the issue.

The failure of. the

board to transfer

to the alternate

breaker

was not of large safety

significance.

Transfer of the board is manually initiated by operators

if power to the board is lost.

There is another

480V shutdown board

on

each unit with the loads divided between

them.

The licensee

subsequently

placed the 480V shutdown board

on the

alternate

supply and on the evening of March 14, continued the

surveillance test.

Again, the inspector

observed

good overall

use of

self checking by TPS personnel.

During preparation to perform

a slow

start of the

C EDG, the inspector observed

a personnel

error on the part

of the

AUO which was identified and immediately corrected

by the

SRO

leading the test.

During a subsequent

step,

an error by the two TPS

workers was also promptly identified and corrected

bP the

SRO.

The

detection of the errors indicated

good attention to detail

on the part

of the

SRO.

Problem Evaluation Reports

(PERs) were initiated to address

the issues.

The inspector also observed that the Unit 3 Control

Room

(CR) operators

utilized good self checking

and adhered to the procedures

during

startup, paralleling,

and shutdown of the

EDG.

Conclusions

Overall conduct of a complex surveillance involving 3EC shutdown board

testing

was good.

Self-checking

and communications

practices

were

observed to be strong.

The

SRO coordinating the testing was well

prepared

and applied excellent supervisory oversight throughout the

test.

The

SRO promptly identified and corrected

two personnel

errors

during the testing.

The investigation

and immediate corrective actions

for an emergent electrical

board switch problem were performed well.

Control

Rod Exercise Testin

Observations

Ins ection Sco

e

71707

61726

During the inspection period, the inspectors

observed

performance of

portions of control rod exercise testing.

Problems

were previously

identified by the licensee

regarding execution of the control

rod

exercise test which resulted in a mispositioned

rod.

That incident was

addressed

in Inspection Report 50-259.260.296/98-01

Section 01.4.

Observations

and Findin s

On March 7,

1998, the inspectors

observed control

room personnel

during

performance of Surveillance

Instruction, 3-SI-4.3.A.2

~ Control

Rod

Exercise Test,

Revision 9.

Shortly after the inspectors

arrived in the

control

room, performance of the surveillance

was stopped for a short

break.

The Peer Checker

and the Reactor

Engineer left the control

room.

After a brief period, the Peer Checker returned

and discussed

restart of

the surveillance activities.

The

RO selected

rod 30-39 and began the

two step insertion from'tep 48 to 46.

At that time, the inspectors

got

the attention of the Unit Supervisor

(US) who was just ending

a

telephone

conversation

and identified to him that the surveillance

was

restarted without the Reactor

Engineer

back in the control

room.

The

US

immediately stopped the operators

performing the testing.

Within

moments.

the Reactor

Engineer entered the control

room.

The

US briefed

the Reactor

Engineer

that the rod movement

was started

and allowed the

surveillance to continue.

.The Shift Manager

was briefed shortly

thereafter

and stopped

performance of the surveillance.

Operations

and

plant management

were notified and responded to the control

room.

Ouring the brief observation of the performance of the surveillance

prior to the break, the inspectors

noted that control

room personnel

demonstrated

an acceptable

level of formality and attention while

performing surveillance activities.

The surveillance instruction in use did not require that the Reactor

Engineer

be in the Control

Room for the movement of rods.

Recent events

in this area

have heightened

the licensee's

sensitivity to this

surveillance activity and specific control rod drive exercise

expectations

were promulgated

as Standing Order OS-0130.

Among the

written expectations

was that the Nuclear Engineer shall

remain in the

affected Control

Room. during the pre-job brief, and while control rods

are being exercised.

There was not

a technical

or safety concern with

the operators

moving the control

rod in accordance with the surveillance

instruction without the Nuclear Engineer in the control

room.

The

problem was limited to a lack of attention-to-detail

on the part of the

operators

performing the test in that they did not ensure that the

Nuclear Engineer

was in the control

room before recommencing

the test.

The Reactor Operator,

Peer Checker,

and Unit Supervisor were

subsequently

rotated to other positions not associated

with the testing.

The licensee restarted testing with the new group of operators.

The

inspectors

observed that the operators

were performing the surveillance

with an appropriate

level of formality and that the operators actively

referenced

the operating instruction.

Licensee

management's

sensitivity

to this issue

was evident.

The licensee also addressed

this issue with

problem evaluation report 980342,

which identified additional

concerns

and documented

thorough corrective actions.

On March 28.

1998.

one of the resident

inspectors

observed

portions of

the Unit 3 control rod exercise test.

The inspector specifically noted

that the formality of the performance

was appropriate

and consistent

with management

expectations.

c.

Conclusions

Licensee

management

promptly and aggressively

responded

to an

NRC

observation that an expectation

contained in a standing order for

control rod exercise testing

was not implemented.

The issue

was

thoroughly reviewed by the licensee.

documented

in the corrective action

program,

and acceptable

corrective actions

were completed.

In general,

the inspectors

have noted increased

Operations

Department sensitivity to

meet management

expectations

during the performance of this testing.

Unit Three Manual Reactor Scram after Recirculation

Pum s Runback

Ins ection Sco

e

71707

93702

The resident

inspectors

observed

and reviewed the actions of control

room operators

following a manual reactor scram due to entering

potential instability Region .1 on the core thermal

power to flow

diagram.

A resident inspector also observed

portions of the plant

cooldown including placing shutdown cooling in service.

Observations

and Findin s

At 11: 12 a.m.,

on April 7,

1998.

both recirculation

pumps

(3A and 3B) on

Unit 3 experienced

a run back to the 28K speed limiter .

The operator s

commenced inserting control rods

and performed 3-SI-4.5.M. l.b, Core

Thermal Hydraulic Stability Flow Decrease,

in accordance with Abnormal

Operating Instruction (AOI) 68-1.

Performance of 3-SI-4.5.M. l.b

indicated that core thermal power/flow was just inside Region

1 of the

core thermal

power to flow diagram.

At 11:16 a.m., the operators

inserted

a manual scram in accordance with TS 3.5.M.2 and AOI 68-1.

One

of the resident

inspectors

responded to the control

room and monitored

operator recovery actions.

The other

resident

inspectors

observed

conditions in the reactor building following the scram.

By examination of control

room chart recorders

arid other indications.

the inspectors verified that reactor vessel

level decreased

to a minimum

of -18 inches before being restored

by the reactor

feed pumps.

Primary

containment isolation equipment

performed

as designed

and no safety

system problems occurred.

The cause of the 3A and

3B recirculation

pumps run back was due to a

loss of power to the 3A and

38 Recirculation

Pump Auxiliary AC Circuits.

A TVA corporate engineer

was taking measurement

in an auxiliary

instrument

room cabinet in preparation

for

a recirculation

pump

controller modification in the upcoming Unit 3 outage.

The corporate

engineer

was briefed by the system engineer to perform

a visual

inspection of the cabinet internals.

He was aware that equipment within

the cabinet

was energized

and was also briefed by the control

room unit

supervisor.

The loss of power to the 3A and

3B Recirculation

Pump Auxiliary AC

Circuits occurred

when the supply breaker

(Unit Preferred

Panel 9-9,

Breaker 603) opened

as

a result of a circuit fault.

When taking

measurements

in the cabinet in the vicinity of a fuse (FUl-68-2A/K4A),

the supply side of the fuse was accidentally shorted to ground by a

metal

measuring

tape

used

by the engineer.

This caused

the supply

breaker to open.

This de-energized

relays

and opened contacts

in the

recirculation

pump speed control circuits which normally bypass the 28K

speed limiter.

As

a result.

the recirculation

pumps experienced

a run

back to 28K speed.

The inspectors

inspected

the interior of the cabinet

and found that the fuse holder for FUl-68-2A/K4A was mounted

on

a metal

backing plate.

The supply side of the fuse was apparently shorted to

the metal backing plate by the measuring

tape

as indicated

by burn marks

on the fuse and plate.

The inspectors verified that controlled drawings

of the involved circuitry supported the postulated

series of events.

One of the inspectors

observed

Incident Investigation (II) team members

questioning the engineer

on his actions.

The team asked

good questions,

including requesting

his input for corrective actions.

The inspector

reviewed II Event Report 98-003814-000

and the Scram Report

(Attachment

1 of 3-AOI-100-1. Reactor Scram).

The inspector

concluded

that the II team performed

a thorough review of the incident and the

lant response

to the scram.

At the close of the inspection period. the

icensee

was developing corrective'ctions

including strengthening of

controls over such evolutions inside electrical cabinets.

Following the manual

scram,

Unit 3 performed

a plant cooldown to

commence

a mid-cycle refueling outage.

This outage

was preplanned

in

the event of a reactor

shutdown in order to replace leaking fuel

assemblies.

A resident

inspector

observed

portions of the plant

cooldown including placing shutdown cooling in service.

The inspector

verified that 3-SI-4.6.A.l. Reactor

Heatup or Cooldown Honitoring, was

being performed during the cooldown.

The inspector observed that

control

room operators

performed

a detailed

peer

check of the shutdown

cooli'ng lineup prior to placing it in service.

Conclusions

Control

room operators

properly inserted

a manual scram after entering

Region

1 of the core thermal

power.to flow diagram following a

recirculation

pump run back.

The run back resulted

when

a breaker

opened in the recirculation

pump control circuitry.

The problem was

caused

when an engineer taking measurements

in an instrumentation

cabinet allowed

a metal tape measure to contact

a fuse holder.

Operator

response

following the scram

was good.

The peer check performed

on the

shutdown cooling lineup was considered

a good practice.

The Incident

Investigation

was thorough in their review of the scram

and equipment

issues.

0 erations

Performance

Issues

Review

Ins ection Sco

e

71707

The resident

inspectors

reviewed operations

performance

issues

which

occurred over the last several

months to determine if a significant

negative trend existed.

The inspectors

requested

that the licensee

provide Tracking and Reporting of. Open

Items

(TROI) data to identify the

problem evaluation reports

(PERs) which were status control issues.

In

addition, the inspectors

considered

other recent

issues of concern.

Observations

and Findin s

The inspectors

developed

a list of operations

performance

issues

from

review of the

PER items identified by the search of the TROI database

and by consideration of other

recent events that the inspectors

were

aware of.

Although the period of review was approximately six months,

most of the items

on the list occurred within the last two months.

It

initially appeared

that an increase in the number of operations

performance

issues

had occurred:

however,

upon review of the individual

items, the inspectors

concluded that the saf'ety significance of many of

the items was minor.

The more significant items on the list were

dispositioned

in NRC inspection reports or will be addressed

through

review of a Licensee

Event Report

(LER).

Half of the more significant

items. were at the beginning of the review period.

In addition,

two

items will be addr essed with an

NRC review of Unit 1 items.

The majority of the items reviewed were identified by the licensee.

The

licensee

noted

an increase

in the number of personnel

errors in the

February

1998 time frame and initiated

a

8 level problem evaluation

report to review this issue.

Additionally, the licensee

informed the

inspectors that

a third party independent

detailed review of Operations

performance

was planned.

Conclusions

The inspectors

concluded that

a recent increase

in the number of

operations

performance

issues

did not constitute

a significant negative

trend.

The safety significance of many of the items was minor and

a low

threshold of problem identification was noted.

0 erations Shift Turnover

Ins ection Sco

e

71707

The resident inspectors

observed

numerous shift turnovers of operations

department

personnel.

Pre-shift turnover meetings

were also observed.

Observations

and Findin s

Requirements

for the shift turnover are described in SSP-12. 1, Conduct

of Operations.

The inspectors

observed

numerous shift turnovers of

operations shift personnel

and compared their performance with the

expectations

described in the procedure.

The turnovers

observed utilized shift turnover checklists

as

a guide for

the turnover process.

These checklists

are contained in O-GOI-300-1,

Operator

Round Logs.

The shift turnover checklists

were detailed

and

contained

good summaries of plant conditions.

Information on the

checklists

included equipment out of service/reduced

status,

equipment

returned to service.

evolutions

and maintenance

in progress,

and other

pertinent plant information.

These checklists

were effective in

E

capturing important plant information and resulted in consistent

information being passed

from crew to crew.

All observed

pre-turnover

board walkdowns by control

room personnel

~

(i.e... unit supervisors'esk

unit operator

and board unit operator)

were

considered detailed.

Pertinent plant information, such

as recent

equipment

problems

and evolutions in progress,

were effectively relayed

to the oncoming watchstander.

Oncoming operator

reviews of specified documentation

(e.g.

~ narrative

log. disabled annunciator

log, etc.) generally satisfied the

expectations of SSP-12. 1.

The inspectors

noted minor discrepancies

in

the manner that two of the four board unit operators

observed

reviewed

the operating logs.

One operator

reviewed the narrative log after

taking the watch.

This was the operators first day back

on shift and

thus

he was expected to review the previous

5 days of log entries.

The

other

operator

was not observed to review any documentation

but

discussed

the logs with the off going board operator.

'he inspectors identified an inconsistency

between the SSP-12. 1

description for auxiliary unit operator

(AUO) turnover requirements

and

the 0-GOI-300-1 turnover checklist.

The SSP-12.1 description states

that the 0-GOI-300-1 checklist documents that review of the narrative

logs has

been performed by the oncoming operator.

However. there was no

requirement

on the 0-GOI-300-1 checklist for the

AUO to review the

narrative logs.

The AUO turnovers

observed did not perform the

narrative log review.

The inspectors

informed licensee

management

of

the discrepancy.

The licensee

plans to revise

SSP-12.

1 to clarify that

AUO review of the narrative log is not required prior to turnover.

The shift turnover meetings

were conducted following individual operator

pre-turnover activities.

The shift turnover

meetings

were led by the

oncoming shift manager

and were formally structured.

Following a brief

discussion of plant status

and recent

problems. all shift personnel

discussed

the status of their individual watch station.

This discussion

included

a summary of the information contained

on the turnover

checklists.

These discussions

were considered

detailed

and thorough.

New operations

department

instructions.

standing orders,

recent

PERs

associated

with operations

and industry events

were also discussed.

Management

expectations

were also routinely stressed

at the meetings.

Support group representatives

(i.e.

~ fire protection, security,

maintenance,

and engineering)

also attended

the shift turnover meetings.

These personnel

provided discussions

of pla'nned activities for the

shift.

The attendance

of the these

personnel

was considered

valuable in

that equipment operational

concerns

are discussed.

Also, conflicts with

lanned activities were occasionally identified based

on the discussions

etween operations

and support personnel.

05

05.1

Conclusions

Attendance of support group representatives

(i.e.. fire protection.

security.

maintenance,

and engineering)

at the shift turnover meeting

was considered

a good practice.

Board walkdowns by operators

were

detailed,

thorough,

and consistent

from crew to crew.

Pre-shift reviews

of required documentation

were generally thorough.

Operator Training and Qualification

Licensed

0 er ator

Re

ua1 ification Pro

ram

Ins ection Sco

e

71001

The inspectors

conducted

a routine.

announced

inspection of the licensed

operator requalification program during the period March 2-6,

1998.

Specific areas of review included requalification examinations,

sampling

methods

used for examination generation,

training feedback,

remedial

training,

and conformance with operator

license conditions.

Observations

and Findin s

The inspectors

reviewed the licensee's

methodology for sampling of the

examination

database

in developing the requalification examinations

for

licensed

Reactor

Operators

(ROs)

and Senior Reactor Operators

(SROs).

The examinations

were developed

and implemented in accordance

with TVA

Nuclear Training Procedure

TRN-11. 10,

"Annual Requalification

Examination

Oeyelopment

and Implementation,"

Revision 2.

The inspectors

examined the licensee's

"Exam Content by Subjects" matrices for the 1996

and

1997 training cycles

and noted that the subjects

covered were in

compliance with the requi rements of 10 CFR 55.41

and 43 as applicable,

and as delineated

in Procedure

TRN-11. 10, Appendix C.

Also. the above

matrices

appeared

to be well balanced

between

what material

was

specifically covered during the training cycle and an approximate

sample

of 20K of need-to-know material that was not covered.

The inspectors

concluded that the licensee's

sample plan was very good.

The inspectors

reviewed

a representative

sampling of the requalification

operating examinations that were administered

in the fall of 1997.

The

simulator

scenario content

and level of difficultywas appropriate to

properly evaluate the competency of the

ROs

and

SROs examined.

The

inspectors

also reviewed

a small sampling of the

1997 written

requalification examinations

and noted,

howevers

a large number of

questions that only required

a fundamental

(simple memory) level of

knowledge in order to answer the questions. 'n addition,

some of the

multiple choice distractors

were easily eliminated without a strong

knowledge in the subject matter.

The inspectors

were concerned that

because all of the examinations

were "open

book ~ " the examinee

could

simply look up the answers without demonstrating

minimal competency

requirements

as operators.

This issue

was discussed

with the licensee

during the inspection

and during the exit meeting of March 6.

1998.

The

licensee

was already

aware that the examination did not fully meet'the

10

standards

of NUREG 1021.

Operator Licensing Examination Standards

for

Power Reactors."

Interim Revision 8.

and as discussed

during the

NRC

Region II sponsored

workshop conducted in January

1998.

The licensee

stated that future examinations

would be written to the higher

standards.

The inspectors

concluded that the examinations

as

administered

were marginally adequate

to discriminate against

incompetent operators;

howevers

a strong training program combined with

a 'lower examination quality may have contributed to the high grades

(approximately

95K average)

that were achieved in 1997.

The inspectors

reviewed remediation activities for two individual

ROs

that failed their weekly written examinations,

for one

RO that

demonstrated

notable weaknesses

on the control

room simulator

.

and for

two crews that failed their weekly simulator examination.

The licensee

documented

the failures,

removed the operators

from licensed duties

until satisfactorily remediated,

and documented

the material

covered

during remedial training.

In all cases,

an examination

was administered

to confirm remediation.

The inspectors

found no problems with the

licensee's

remedial training process.

Element (5) of the Systems

Approach to Training,

as defined in

10 CFR 55.4. requires evaluation

and revision of training based

on the

performance of trained personnel

in the job setting.

The licensee's

training staff provided the inspectors with objective evidence that this

approach

was being taken at the Browns Ferry Nuclear facility.

The

inspectors

reviewed several

simulator exercise

guides which incorporated

events

and incidents that had occurred at this facility.

In addition.

the inspectors

randomly selected

a Browns Ferry incident from the NRC's

tracking system.

On April 1,

1997. control

room operators failed to

promptly reset

a locked recirculation

pump scoop tube under runback

conditions.

The inspectors

noted that this incident was addressed

in

Simulator Exercise

OPL173S194,

dated April 28,

1997.

The inspectors

concluded that the licensee

had implemented

a feedback

process

as

required

by 10 CFR 55.4.

The inspectors

reviewed the licensee's

program for reactivating inactive

operator

licenses

and assessed

compliance with 10 CFR 55.53(e)

and (f).

The inspectors identified problems with the licensee's

process to ensure

operators

gained the proper quantity and. quality of practical

experience

in order to maintain

an active license

or to reactivate

an inactive

license,

as required

by NRC regulations.

10 CFR 55.53(e) states.

in part, "If a licensee

has not been actively

performing the functions of an operator

or senior operator,

the licensee

may not resume activities authorized

by a license

issued

under this part

except

as permitted by paragraph (f) of this section."

10 CFR 55.53(f)

states,

in part, "If paragraph

(e) of this section is not met

~ before

the resumption of functions authorized

by a license

issued

under this

part,

an authorized

representative

of the facility licensee shall

certify the following: ... (2) That the licensee

has'completed

a minimum

of 40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> of shift functions under the direction of an operator or

senior operator,

as appropriate,

and in the position to which the

11

individual will be assigned.

The 40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> must have included

a complete

tour of the plant and all required shift turnover procedures."

.

The inspectors

reviewed the License Status

Change

Forms, control

room

logs, and,the vital area

access

records for 13 operators that had

reactivated their licenses

at some time during the period March 11,

1996, to January

27 '998.

A review of the vital area

access

records

for each reactivation period resulted in total hours ranging from a

minimum of 28.2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> to a maximum of 37.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />, with the average

being

32.6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.

These totals were compiled using generous

acceptance

criteria which gave credit for short time intervals of as little as

one

minute spent

by the operators within a control

room boundary.

The total

hours also included time in-plant making tours and, in some cases,

shift

turnover.

Nevertheless,

the inspectors

found that

12 operators

were

significantly short of the 40-hour minimum requirement to reactivate in

the position to which the individual was to be assigned.

The inspectors

also were unable to verify 'that

an individual stood

a parallel watch in

the position to which he was to be assigned

given the large number of

vital access

area entries

and exits that occurred during the stated

reactivation periods.

The inspectors

determined that, in each of these

12 cases.

an authorized representative

of the facility incorrectly

certified that the operators

had completed

a minimum of 40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> of

shift functions

under

the direction of an

RO or SRO and in a position to

which the individual will be assigned.

The inspectors

noted that circumstances

surrounding this problem were

similar to those associated

with a previous violation *that was

identified in December

1994.

This was Violation

50-259,260,296/94-11-01.

"Requirements for reactivation of

operators'icenses

were incorrectly certified."

The corrective actions taken

as

a

result of the previous violation were not effectively implemented to

preclude repetition.

In view of the continued

problems identified in the licensee's

operator

license reactivation

program,

the inspectors

requested

the licensee to

determine if inappropriately reactivated

operators

were performing

licensed activities at the time of this inspection

and over the past

year.

The licensee

found several

instances

where operators fulfilling

the minimum shift crew requirements of TS 6.2.2.a

were not holding

properly reactivated

licenses.

The inspectors

also questioned

the

functions performed by operators while maintaining their licenses

active.

10 CFR 55.53(e)

requires,

in part,

"To maintain active status,

the licensee shall actively perform the functions of an operator or

senior operator

on

a minimum of seven 8-hour or five 12-hour shifts per

calendar

quarter ." It was determined that

some of the operators

were

not actively performing the functions of operators

or senior

operators

as defined in 10 CFR 55.4 during shifts which were credited

towards

maintaining active license status to satisfy the requirements of

10 CFR 55.53(e).

For example,

operators

were given credit for

performing the functions of the shift technical advisor,

which was not

a

position requiring

a license.

As

a result. certain operators

were

performing the functions of active licensed operator or senior operators

12

while their license

was in an inactive status.

Failure to fulfillthe

minimum shift crew requirements

is

a violation of TS 6.2.2.a

(50-259.260 '96/98-02-01).

The licensee

promptly removed the operators

and senior operators with

inactive licenses

from licensed positions

on the watch list, and

implemented detailed procedures

to properly control

and document

operator license activation/reactivation to meet the requirements

of'0

CFR 55.53(e)

and (f). "Conditions of Licenses."

Conclusions

The inspectors

concluded that the licensed operator requalification

program was adequate with respect to the examination question

sampling

process,

remediation training. operating examination content validity.

and feedback of plant events

and incidents into the training curricula.

However, the written examinations

contained questions of marginal

discriminatory value.

and therefore,

did not fully meet the standards

established

in NUREG-1021,

Interim Revision 8.

The licensed operator

activation/reactivation

process

was incorrectly

implemented resulting in operator licenses

being certified active when,

in fact, they were not.

As a results

on several

occasions

the licensee

did not fulfillthe TS-requi red minimum shift crew requirements

for

actively licensed operators while the plant was in operation.

A

violation was identified by the inspectors for failure to comply with

TS 6.2.2.a.

This was identified as violation 259,260,296/98-02-01,

Failure to Meet Minimum Shift Crew Requirements.

Observation of Simulator Trainin

Ins ection Sco

e

71707

Two of the resident

inspectors

observed

several

control

room simulator

training sessions

for licensed senior

and reactor operators.

In

accordance

with Inspection

Manual

71707 'he effectiveness

of the

observed training was assessed.

The resident

inspectors

were assisted

by two Region II Operator

Licensing Branch inspectors.

Observations

and Findin s

The inspectors

observed three sessions.

with one being the

same scenario

presented

to two different crews of operators.

The scenarios

included

extensive

use of the Emergency Operating

Procedures

(EOPs)

and were

challenging in their overall complexity.

In all of the. scenarios,

the

crew successfully

recognized the major events. utilized response

procedures,

and stabilized the unit.

The inspectors

observed that the operators

were knowledgeable

regarding

details of plant equipment

performance. 'or example,

response

to

alarming annunciators

in the initial phases of the scenarios

was prompt

and aggressive.

On several

occasions,

based

on their experience,

the

13

reactor operators

proposed

sound

recommendations

to the Senior Reactor

Operators

(SROs) well in advance of required procedural

actions

The inspectors

observed that the operators rigidly adhered to management

expectations

regarding three way communications early in the scenarios,

but with increasing intensity of conditions.

the communications

were not

as consistent.

Overall. the Unit Supervisors

adequately briefed the

operators

at appropriate intervals during the'cenarios.

However, there

were

a few occasions

in which the briefings were not effective.

The inspectors

observed the training critique sessions

for the sessions.

The inspectors

noted that several

errors or performance

issues

were not

thoroughly addressed

during the critiques.

The inspectors

observed that

a board operator failed to detect that

a emergency diesel

generator

had

not started during two separate

checks of the 4kV shutdown board

indications.

While this was addressed

during the critique, the fact

that it was detected

on

a subsequent

check

was the focus rather

than'mproving

future performance.

In several

instances,

operators

volunteered

areas

in which their performance

needed

improvement

and the

training instructor did not sufficiently highlight the deficiency.

It

appeared to the inspectors that the training personnel

were not

consistently enforcing high standards

of proficiency during the critique

sessions.

Additionally, management

expectations

regarding self-checking

were not being rigidly enforced.

In the critiques.

the Shift Manager

was relied upon to provide the

majority of input regarding

crew performance.

It appeared to the

inspectors that it would be difficult for the Shift Manager

. during

complex plant conditions'o fully participate in the training and

identify all problems.

These observations

were discussed

with the

BFN Training Manager

and

Operations Training Manager.

On March 31,

1998, the senior resident

inspector

reviewed the Institute

of Nuclear

Power Operations

(INPO) Accreditation Evaluation Report dated

February 26,'1998.

The National Nuclear Accreditation Board renewed the

accreditation of six BFN training programs.

No major adverse

concerns

were identified in the report.

The inspectors

noted that the report

contained

some negative observations

involving poor identification and

addressing

of individual operator

performance

problems during simulator

critique sessions.

,c.

Conclusions

In several

observed control

room simulator training scenarios,

the crew

successfully

recognized the major events. utilized response

procedures,

and stabilized the unit.

In general

operator performance

issues

such

as

use of procedures

and communications

were addressed:

however,

management

expectations

for self-checking were not consistently

emphasized.

Ouring observation of the critique sessions,

the

inspectors

noted several

examples

which indicated that the training

08

08.1

Ml.l

14

personnel

were not consistently enforcing high standards

of overall

proficiency.

Miscellaneous

Operations

Issues

(92901)

Closed

Licensee

Event

Re ort

LER

50-296/97-005-00:

When

a Valve was

Malfunctioning,

an

LCO was not Entered.

This event

was discussed

in IR

97-09 and

IR 97-10.

Violation 296/97-10-03,

Failure to Complete

TS

Action for Inoperable Containment Isolation Valve was issued.

No new

issues

were identified in the LER.

This

LER is closed.

II. Haintenance

Conduct of Maintenance

Standb

Gas Treatment

SBGT

S stem Filter Leak Testin

Ins ection Sco

e

61726

71707

On Harch 19.

1998,

one of the resident inspectors

observed

the

performance of portions of Surveillance Instruction O-SI-4.7.B.4,

Standby

Gas Treatment

(SBGT) System In-place Leak Test, of High

Efficiency Particulate Air

(HEPA) Filter Banks

on the "C" train of

SBGT.

The test is intended to implement the requirements of Technical Specification 4.7.B.2.b

when performed with other tests.

Observations

and Findin s

Portions of O-SI-4.7.B.4 had been successfully

performed during the

previous

day.

Dioctylphthalate

(DOP) testing of the upstream

HEPA

filter in the "C" train of SBGT had been completed.

Beginning at Step

7.13, the procedure

involved

DOP testing of the downstream

HEPA filter.

DOP testing of the downstream

HEPA filter had been unsuccessfully

attempted

during the previous evening shi.ft.

Discussions with workers

indicated that the testing

was not successful

because

incorrect ports

on

the

SBGT train'had

been used.

The inspector

noted that the maintenance

workers

had ensured that the prerequisites

for the'testing

had been

completed before attempting the test again.

For the test,

a

DOP generator is used to inject

DOP solution into the

filter train upstream of the filter to be tested.

Test equipment is

used to determine the leakage of the

HEPA filters by measuring

how much

of the

DOP is removed

by the filter assembly.

The inspector

observed

several

unsuccessful

attempts to perform the testing of the downstream

filter.

The following observations

were made:

The ports for the testing

(DOP injection point and sensing points

for the monitoring equipment)

were not labeled to match the

procedure.

The equipment for the sensing lines for the

DOP test equipment

was

not standardized.

A copper tubing extension

was constructed

by

15

skill of the craft -on the spot" and used for the "upstream"

sensing line.

This extension

and its placement

in the train was

revised in attempts to obtain

a valid test.

~

At least

one attempt

was unsuccessful

because

the

DOP generator

did not have sufficient

DOP liquid loaded into it.

Although a

sightglass

is available,

the worker s were not familiar with what

the level should be.

The procedure did not address this subject.

~

After several

attempts.

a second

DOP generator

was obtained

and

both generators

were used to inject

DOP into the system

simultaneously.

The procedure did not indicate

how to ensure that

sufficient

DOP was injected into the system.

The inspector

noted

that step

9 of the test equipment procedure stated that the actual

upstream concentration of DOP would be indicated but no minimum

value or typical value was known.

The inspector noted that the

DOP

concentration visually appeared

low.

~

The workers were familiar with the operation of the TDA-2G

analyzer

used to measure

DOP concentrations

in the filter train.

They actively utilized Attachment

2 of the Surveillance

Instruction (SI) which provided step

by step guidance

on how to

operate the equipment.

~

The workers immediately recognized

unexpected test equipment

responses

and were not willing to accept

performance that did not

match the description in the procedure.

~

After about

4 attempts,

the maintenance

workers contacted

a system

engineer for assistance.

After several

more attempts

and

additional engineering

involvement, the

procedure

was revised to

utilize a different upstream injection port and the ports were re-

labeled.

Subsequently,

the test was completed.

~

Torquing of the

DOP injection port cover

was not addressed

in the

DOP test procedure.

The cover

was re-installed but it was not

torqued.

The inspectors

noted that other

SBGT procedures

had

torquing requirements

for this cover.

The system engineer

acknow'ledged

the inconsistency

and

PER 980503 was initiated.

Skill of the craft was heavily relied upon to complete this testing.

Equipment

was not standardized

and labeling was not good.

The

procedure, if implemented strictly as written'ould not be used to

successfully

perform the test (the injection point was apparently too

close to the filter).

Consequently.

the inoperability of the "C" train

of SBGT was extended at least

18 hours2.083333e-4 days <br />0.005 hours <br />2.97619e-5 weeks <br />6.849e-6 months <br />

beyond the scheduled

maintenance

period.

TS require that written procedures

be established

and

maintained for surveillance testing of safety related equipment.

NRC

'nspection

Report 97-08 describes

NRC observation of other

SBGT testing.

The inspector

had noted reliance

on skill of the craft to satisfactorily

complete that testing

as well. but the major focus

had been issues

involving orientation of an instrument probe.

~ ~

16

On March 24. the inspector

reviewed the vendor manual for the

DOP

generator

used in the test.

The generator

was

a Air Techniques

TDA-6A

Aerosol Generator.

The inspector identified that the manual

indicated

that the generator capacity

was for systems

up to 500 cfm

(cubic feet

per minute).

Since the flowrates in the

SBGT systems

are

much higher.

(9.000 cfm) the inspector

questioned

the system engineer

about the

generator.

Section 5.3.5.2 of the

UFSAR describes

SBGT system'esting.

The

UFSAR specifically states that the aerosol

generator is capable of

supplying sufficient

DOP to test for leaks using the 9,000 cfm design

flow of one

SBGT train.

Subsequently.

the system engineer

confirmed

that the incorrect

DOP generator

had been

used for the testing.

Step

5.1 of O-SI-4.7.B.4 lists the equipment to be used

as

a Air Technique

.

generator

Model TDA-5A or equivalent.

The TDA-6A is not equivalent to

the TDA-5A model.

The incorrect model

DOP generator

was used for DOP

testing of all the

SBGT systems

and the Control

Room Emergency

Ventilation (CREV) system.

PER 980507

was initiated to address

the

issue.

TS -6.8. 1.1.c requires that written procedures

shall

be

established.

implemented.

and maintained for surveillance

and test

activities of safety-related

equipment.

Section 5. 1 of Surveillance

Instruction O-SI-4.7.B.4,

Standby

Gas Treatment

System In-Place

Leak

Test of High Efficiency Particulate Air Filter Banks,

and Section 5. 1 of

Surveillance Instruction O-SI-4.7.E.2.A, Control

Room Emergency

Ventilation System In Place

Leak Test, specifically state that an Air

Techniques

Incorporated

Model TDA-5A (or equivalent) Dioctylphthalate

(DOP) generator is to be used for the tests.

This deficiency is

identified as Violation 259,260,296/98-02-02,

Failure to Follow High

Efficiency Particulate Air Filter Testing Procedures.

Preliminary analysis

by engineering

indicated that the testing,

although

not performed in accordance

with the

recommended

methodology,

was

a

valid test of the filters.

Licensee

management

directed that the proper

capacity

DOP generators

be obtained

and the testing

be performed again

as

soon

as practical.

Larger capacity

DOP generators

were expeditiously

obtained

and the testing

was subsequently

performed again

on the

SBGT

and

CREV systems.

The inspector

observed that extensive engineering

involvement was necessary

to complete the testing.'he

licensee

determined that the smaller

DOP generators

had been

used for testing of

the

SBGT and

CREV filters for at least the previously performed test

prior to the most recent.

The licensee

provided

a summary of an evaluation of using the lower

capacity

DOP generator

on the surveillance test.

The evaluation

indicated that the

DOP concentration

was sufficient to ensure that with

.005 percent penetration of the filter the downstream

DOP levels would

be within the sensitivity of the Model TDA-2G penetrometer.

The

evaluation stated that the 100 micrograms

per liter at 150

CFM generator

capacity correlated to 1.6 micrograms per liter upstream of the filters

at 9,000

CFM in the

SBGT trains.

The inspector noted that the

evaluation

assumed

uniform dispersal

of the aerosol

upstream of the

filter.

17

The inspector

reviewed portions of American National Standard Institute

(ANSI) N510-1975. Testing of Nuclear Air-Cleaning Systems.

TS 3.7.B.2

states that

DOP testing of the filters will be performed in accordance

with ANSI N510-1975.

The inspector noted that Section 10.4 of the

standard

stated that

DOP generator

capacity shall

be specified in the

test procedure

and shall

be sufficient to produce reliable penetrometer

readings at system penetrations

as low as 0.005 percent.

The inspector

had observed during the test that the

DOP did not appear to be well

mixed with the air flow prior to traveling through the

HEPA filter.

The

inspector

noted that Section

9 of ANSI N510-1975 specifically states

that an air-aerosol

mixing uniformity test is necessary.

This test is

used to verify that the

DOP injection and sample ports are located

such

that proper

mixing of the challenge

aerosol

in the air approaching

the

filter. occurs.

On April 6,

1998. the inspector

asked for the results of

the testing to ensure the proper ports were used.

On April 9,

1998, the

BFN Vice President

discussed

the status of the

issues with the Senior Resident

Inspector

(SRI).

At that time, the

licensee

was searching for the

SBGT systems

aerosol

uniformity test

data.

Licensee indicated that the test

was possibly completed

under

a

previous specification.

Documentation for the

CREV system distribution

test

was found and licensee

subsequently

informed the inspector that the

latest

DOP testing of the

CREV system matched the configuration used in

that test.

As of April 9. plant management

did not consider the plant

in a nonconforming status.

Management

concluded that the most recent

HEPA testing

done had been satisfactorily completed.

Essentially,

the

justification was that so much

DOP was injected that it must have been

distributed adequately.

The inspector

discussed

with plant management

the regulatory concern that it was not clear that the latest testing

was

adequate.

The SRI also discussed

status of issues with Region II

management.

On Apri 1 10,

1998, the licensee

developed

Technical Instruction TI-370

which provided instructions for performing aerosol

dispersion uniformity

testing

and

HEPA filter DOP testing.

A manifold of plastic pipe was

constructed for DOP injection and sampling in accordance

with NUCON

drawings

and instructions.

The manifold was installed into the filter

train for dispersion of DOP prior to the downstream

HEPA filter.

A

NUCON representative

advised the licensee

on details of testing

and ANSI

N510-1975 requirements.

The SRI observed

most of the testing

on "A"

SBGT train.

The SRI observed

assembly of the manifold and inspected

both

HEPA filter banks.

The filters appeared

to be in good condition

and properly mounted.

By visual examination through

a port. the

inspectors

observed that there

seemed

be more even dispersion of DOP

upstream of the downstream

HEPA than during previous testing.

On April

12,

1998, the licensee

completed testing per TI-370 on all three

SBGT

trains.

The results indicated that all the

HEPA filters had acceptable

efficiency and there

was not excessive

bypass

flow.

TS 3.7.B.2.a

requires that testing of the filters be performed in

accordance

with ANSI N510-1975.

The procedure

was not adequate

to

ensure that the leak testing of the downstream filters was conducted in

18

accordance

with the ANSI Standard.

The subsequent

testing confirmed

that the dispersion of the aerosol

for testing of the upstream

HEPA

filters was adequate

using the previous test method.

The

UFSAR and

TS

state that both filters are to be tested in accordance with the ANSI

standard.

This issue is identified as Violation 259,260,296/98-02-03,

Inadequate

Testing of Downstream Standby

Gas Treatment

HEPA Filter.

Conclusions

The licensee did not initially perform an aggressive

review of the

inspector's

concern that

SBGT testing relied upon the skill of the

maintenance craft to work around procedural

obstacles.

The

NRC

identified that the model of DOP generator

used for testing of the

SBGT

and

CREV systems

was not equivalent to that model required

by the

procedure.

A violation was identified for failure to follow testing

procedures.

(Violation 259,260,296/98-02-02.

Failure to Follow High

Efficiency Particulate Air Filter Testing Procedures).

Additional

NRC

review identified that the procedure for testing the

SBGT downstream

filter did not meet the requirements of ANSI N510-1975 as required by

TS.

( Violation 259,260,296/98-02-03.

Inadequate

Testing of Downstream

Standby

Gas Treatment

HEPA Filter).

Hi h Pressure

Coolant In ection

HPCI

Exhaust Line Ru ture Disc

Preventive

Maintenance

Ins ection Sco

e

62707

One of the resident

inspectors

observed portions of the work activities

involved in replacement of the HPCI exhaust line rupture disc

assemblies.

The inspector also observed

portions of the American

Society of Mechanical

Engineering

(ASME) Section

XI inspection of the

removed disc assemblies.

Findin s and Observations

The preventive maintenance

was performed in accordance with Work Order

(WO) 97-004682-000

and Mechanical

Preventive

Maintenance

Instruction

MPI-0-073-TRB001,

HPCI Turbine Preventive Maintenance.

Section 7.5 of

the MPI, HPCI Turbine Exhaust

Rupture Disc Replacement,

contained

appropriate

guidance to properly perform the work.

The inspector

verified that the work instructions incorporated

guidance

included in

the vendor reference

manual;

BfN-VTD-F103-0050, Installation and

Maintenance

Instructions for Fike Rupture Disc Assemblies.

The

inspector also reviewed documentation

and the nameplates

on the new disc

assemblies

to verify that the replacement

discs were the correct

pressure

value.

The inspector

observed that maintenance

personnel

were

careful to adhere to cleanliness

requirements

during handling of the

'ssemblies.

Technical

Instruction TI-362, Inservice testing

Program of Pumps

and

Valves, sets forth the details of the

BFN inservice testing program.

The inner

HPCI system rupture discs are listed to be visually inspected

19

in accordance

with Surveillance Instruction 2-SI-3.2. 19. Inspection of

ASHE Section

XI Rupture Discs.

The inspector

observed portions of the

performance of the inspection.

Step 6.3 of 2-SI-3.2. 19 describes

criteria for the "as-found

condition of the disc.

The inspector

noted

that the engineer

was performing the inspection for cracks,

dents,

or

excessive

corrosion

by visually examining the exterior surface of the

vacuum support

component of the disc assembly.

The disc assemblies

consist of a vacuum support piece.

two rupture discs'nd

a dust cover

spot welded together in an assembly.

Host of the rupture disc material

.

is not visible behind the vacuum support piece.

The inspector

asked if

the assemblies

were disassembled

so that an examination of the rupture

disc material could be performed.

Subsequently,

the licensee

disassembled

and

removed the inner disc assembly

and identified that the

rupture disc material

had pitting, indications of corrosion,

and

some

cracking.

Although the holes were very smally through wall penetrations

existed in both of the discs.

The observed conditions failed the as-

found criteria in 2-SI-3.2. 19.

At the close of the report period. the

licensee

was performing

a closer

review of the degradation.

The process utilized to determine the as-found conditions of the discs

was not adequate

since the disc material itself was not examined.

Degradation of the disc material

was significant since the rupture

setpoint could be adversely affected.

Additionally, the inspector noted

that drawing 2-4E812-1-ISI depicts the inner disc assembly

as the ASHE,

code class 2'oundary.

Through wall defects of such components

are

degradations

and should

be evaluated.

The licensee

examined the rupture discs for the Unit 3 HPCI system

on

April 14,

1998,

and identified that no degradation

was present.

Additionally, the licensee

noted that the Unit 3 disc assembly contained

only one disc instead of the two thinner material discs

found in the

Unit 2 assembly.

At the close of the inspection period. the licensee

was reviewing this issue with the vendor.

The RCIC system discs are

provided by the

same manufacturer

but are smaller and

may not be similar

in details of assembly.

The inspector

noted that Section 1.3.4.2 of ANSI/ASHE ON-1 states that

classes

2 and

3 nonreclosing

pressure relief devices shall

be replaced

every five years unless historical data indicates

a requi rement for more

frequent replacement.

The vendor manual

contained

a statement

recommending that the discs

be replaced

every year under normal

operating conditions.

Licensee engineers

indicated to the inspector

that this was interpreted to apply to systems

which are normally

operating.

not systems

operated for very short time periods.

Surveillance testing of the HPCI system

had been completed

satisfactorily previous to the replacement of the disc.

Normal

HPCI

exhaust line pressures

are well below the rupture setpoint of the disc.

It appeared that the licensee's

actions were in compliance with

ANSI/ASHE OH-1 requirements

for periodic replacement of the discs.

The

major concern is that the degraded condition would not have been

'

20

identified and evaluated.

Violation 260/98-02-04.

Failure to Identi fy

Degraded

HPCI Rupture Discs addresses

this issue.

Conclusions

Periodic replacement of the High Pressure

Coolant Injection System

turbine exhaust

rupture disc assembly

was performed satisfactorily

except that the as-found inspection process

was not adequate

to identify

that the disc material

was degraded.

The licensee did not identify the

degradation until the inspector

questioned

the inspection

method.

(Violation 260/98-02-04,

Failure to Identify Degraded

HPCI Rupture

Discs).

Fix-It-Now Team Observations

Ins ection Sco

e

62707

The resident inspector

observed

Fix-It-Now (FIN) team work to ensure

that'the work was performed within specific procedural

guidelines.

Specifically, the inspectors

focussed

on implementation of Site Standard

Practice SSP-lZ.3,

Equipment Clearance

Procedure for the performance of

work not under the control of a clearance.

Observations

and Findin s

On March 2,'998,

an inspector

observed the FIN team's troubleshooting

efforts to determine the cause of the refuel

zone supply outboard

isolation damper,

2-HS-064-0005. failing to indicate full closed

when

the fan was

removed from service.

The troubleshooting effort was well

controlled with control

room operators

aware of the FIN team's

planned

activities and involved in the damper manipulation.

FIN crew

troubleshooting

determined that the associated

limit switch, 2-LS-064-

0005,

needed to be replaced.

The FIN crew stopped troubleshooting

activities and

a Work Order

(WO) was developed to address

the limit

switch problem.

On March 12,

1998.

an inspector observed

the FIN team troubleshooting

a

problem with the

3B Steam Packing Exhauster

Breaker.

The

troubleshooting

was conducted in accordance

with Work Order

(WO)

98-002759-000.

A thorough briefing was held prior to the work.

The FIN

team

SRO actively supervised

the work.

The troubleshooting

involved

opening electrical

breaker

enclosures

and monitoring equipment

performance

as control switches

were operated.

The workers utilized

proper caution regarding the proximity to energized electrical

equipment.

At the conclusion of the troubleshooting efforts, the work

was stopped

pending additional

maintenance

planning.

On March 24.

1998.

an inspector

observed portions of FIN crew

maintenance activities to repair

3C2 waterbox screen

linkages.

The

maintenance

work was performed with the breaker

handswitch for the

normal

power supply to the Condenser

Tube Cleaning

System

3C2 in the off

position with an Assistant Unit Operator 'stationed in the area to ensure

21

the system

was not energized.

The work performed required maintenance

personnel

to replace portions of the linkage between the motor operator

and the screen

mechanism.

Discussions with the licensee

indicated that

this work would not be performed with the motor operator energized

due

to the risk to personnel

safety.

Site Standard

Practice,

SSP-12.3,

Equipment Clearance

Procedure,

described the performance of work not under the control of a clearance.

The observation of work on March 24, could not be directly correlated to

the exceptions

allowed by the procedure.

The inspector discussed

the

observations

with the Operations

Superintendent.

Subsequent

discussions

with licensee

management

confirmed the FIN team practice of using

operations

personnel,

in some cases,

to ensure that the component

was

maintained in the safe position instead of using

a clearance to

reposition the component.

The licensee is reviewing the procedure to

determine if this is acceptable

implementation of the procedure

and

management

expectations.

Pending

NRC review of the licensee's

evaluation, this item is identified as Inspection Follow-up Item (IFI)

260,296/98-02-05.

Use of Personnel

in Place of Equipment Clearances.

The inspector also reviewed the evaluation associated

with a problem

evaluation report which was associated

with work that the FIN team

performed.

Problem Evaluation Report

(PER)

980035 described

work that

was being performed

on the sewage lift station

and resulted in a sewage

overflow.

Work was performed

on the lift station in the absence

of

individuals from the Environmental

Section

who were familiar with the

lift station operating controls.

The lift station

was apparently left

with the controls in a configuration which did not allow the remaining

pump to operate automatically at some time during or following the

Clearance

replacement.

The inspector concluded that deficiencies in

this incident did not involve an inappropriate decision to perform

maintenance without a clearance.

Conclusions

The inspector questioned

the procedural

guidance

and implementation

regarding the use of personnel.

in some cases,

to ensure that

a

component

was maintained in the safe position instead of using

a

clearance.

Licensee

management

is reviewing the practice to determine

if procedural

guidance is appropriate

and management

expectations. were

met.

Additional

NRC review of the licensee's

evaluation is necessary

( Inspection Follow-up Item ( IFI) 260,296/98-02-05,

Use of Personnel

in

Place of Equipment Clearances.)

Residual

Heat

Removal Service Water

Pum

Re lacement

Ins ection Sco

e

62707

One of the resident

inspectors

reviewed work associated

with the

C3

Residual

Heat

Removal Service Water

(RHRSW)

pump replacement

and the

C2

RHRSW pump strainer

replacement.

The inspector

reviewed selected

vendor

and licensee

documentation to verify that activities were acceptable.

b.

Observations

and Findin s

22

M8

M8.1

The inspector

reviewed completed work order

(WO) packages

for

WO

98-002355-000

and 98-002013-001

and noted minor documentation

discrepancies.

The licensee

immediately addressed

discrepancies

associated

with WO 98-002355-000

and documented

the issues

in problem

evaluation report

(PER) 98-003901-000.

The inspector

observed

replacement of the

C2

RHRSW pump into position in

the

pump foundation hole and noted that workers were careful

and

appropriately attentive to the activity.

Following removal of the

C3

RHRSW pump head to transfer it to the new

replacement

pump. the inspector noted that significant shaft wear was

apparent

on the old pump shaft in the area of the

pump packing.

A

problem evaluation report

(PER 980521)

was initiated to address

the

wear.

The licensee also removed the packing from the

C2

RHRSW pump for

inspection of the shaft.

The inspector noted that although

some wear

was evident, it was substantially less than that identified on the

C3

pump.

The wear on the

C2

RHRSW pump was determined to be acceptable

and

the

pump was reinstalled.

While reviewing vendor documentation.

the inspector

questioned

a

statement

in the vendor.'s bolt torquing procedure

(BFN-VTD-8580-0160).

The vendor manual stated that all external bolting on subassemblies

or

pumps shipped

assembled,

must be retorqued to specified values before

installation.

The inspector noted that this requirement

was not

included in the work order step text for the

C3

RHRSW pump which was to

be replaced.

The licensee

contacted

the vendor who subsequently

issued

a letter to the licensee

documenting that if the pump has not been

disassembled,

there was

no need to retorque the bolting prior to

installation.

The inspector verified that the stainless

suction strainer.

which

replaced

a carbon steel strainer

on the

C2 and

C3

RHRSW pumps,

was

described

as

an option in the material of construction section of the

vendor technical

manual

(BFN-VTD-.8580-0180).

In addition, the inspector

reviewed design

change notice V39888A which evaluated

the change of

material to stainless

steel.

No problems were identified.

Conclusions

Major maintenance activities on two residual

heat

removal service water

pumps were conducted well.

Placement of the

pump assemblies

was

performed carefully and actions to address

shaft wear were good.

Miscellaneous

Maintenance

Issues

(62707,

92902)

Closed

Licensee

Event

Re ort

LER

260/97-004-00:

Technical

Specification Survei llances

Were Not Performed

During Refueling Outage

Time frames.

This

LER addresses

two examples

in which surveillance

C

23

testing which TS required to be performed "during

a refueling outage"

was performed with the unit at power.

Violation 260/97-09-01,

Functional Testing of Snubbers

While not in'Refueling Outage

addressed

the first example

and remains

open pending

NRC review of corrective

actions.

The other

example involved suppression

chamber to reactor

building vacuum breakers

and was identified by the licensee.

The

licensee

reviewed other

TS testing requirements

and found no other

examples of improperly scheduled testing.

The

LER concluded that

testing of the components

at power did not adversely affect plant

safety.

The

LER is closed.

Additional

NRC review of corrective actions

will be performed for closure of the violation.

H8.2

Closed

Licensee

Event

Re ort

LER

260/97-008-00:

Hain Steam Safety

Valves Exceeded

Technical Specification

(TS) Required Setpoint Limit as

a Result of Pilot Valve Disc/Seat

Bonding and

Closed

Licensee

Event

Re ort

LER

296/97-003-00:

Hain Steam Safety

Valves Exceeded

Technical Specification

(TS) Required Setpoint Limit as

a Result of Disc/Seat

Bonding.

These

LERs address test results obtained

in March 1997 and

December

1997 which indicated that 5 of the

13 Unit 2

valves

and

11 of the

13 Unit 3 valves failed to meet .the

TS setpoint

tolerance of +/- 11 psia.

Some valves lifted below the setpoint

tolerance.

while others were above the allowed setpoints.

Prior to

plant operation,

the Safety Relief Valve (SRV) pilot valve cartridges

were replaced with newly certified cartridges.

The cause

was attributed

to the generic problem of corrosion bonding at the pilot valve disc/seat

interface

on two stage Target

Rock valves.

There has

been

numerous

previous

LERs for such conditions at

BFN.

The issue is still under

review by the Boiling Water Reactor

Owner Group

(BWROG)

SRV Drift Fix

Development

Committee

and the manufacturer.

BFN continues to

participate in the

BWROG evaluation for a permanent solution to the

problem.

Some of the failed pilot cartridges

were of the satellite disc

material

and

some were of the platinum-satellite material.

BFN has

installed modifications which minimize the effects of setpoint drift

by'lectrically

actuating the

SRVs through use of a pressure

switch.

Additionally, BFN has requested

a TS revision to allow the setpoint to

be +/- 3 percent.

The

LERs addressed

the safety consequences

of the

setpoint drift and concluded that

TS safety limits would not have been

exceeded

during operational

events.

The resident inspectors

have also

.discussed

the

BFN safety valve performance with Nuclear Reactor

Regulation

(NRR) personnel

tasked with monitoring the generic corrosion

bonding issue to ensure that the licensee is completing expected

actions.

.These

LERs are closed.

M8.3

Closed

Violation 260 296/96-10-02:

Inadequate

Supervisory Oversight of

EDG Painting Activities.

The licensee's

response

to the violation.

dated

December

6,

1996, stated that the deficiencies

were caused

by

failures to meet

management

expectations

regarding oversight of a

maintenance activity.

The painting was stopped after the issues

were

identified and increased

supervisory attention

was provided prior to

continuation of the painting.

A specific "Painting Expectations"

I

24

document

was issued

as

a Maintenance Night Order.

The resident

inspectors

have been closely monitoring the effectiveness

of supervisory

oversight during the

12 year maintenance activities

on the

EDGs.

Inspection Reports

97-12 and 98-01 contain descriptions of inspection

observations.

The inspectors

have noted that maintenance

supervision

has

been consistently actively involved in the work.

During observations

of

the work, the

inspectors

have noted the performance of selected

requirements

set forth in the "Painting Expectations-

paper.

Through reviews of Cause Determination Evaluations

(CDEs) to address

Maintenance

Rule requirements for a containment isolation valve failure;

the inspectors

noted that deficient painting was involved in that issue.

On December 16,,1996,

valve 3-FCV-64-34 failed to close within the

required time during testing.

Problem Evaluation Report

(PER) 961716

was initiated.

The

PER was

a "C" level

and was closed to Work Request

(WR) 96-008224.

The inspectors

noted that the description of work

performed

on the

WR indicated that paint had been applied incorrectly to

a seal

over

a vent valve.

,The

WR indicated that the paint was removed

to restore the valve to proper operation.

After additional

review, the

inspectors

concluded that the primary cause of this instance of

misapplied paint was probably not a lack of overall supervision.

In

this specific case, it was not so obvious that the paint should not have

be applied to the particular part.

The inspectors

discussed this issue

with Nuclear Assurance

personnel

from a perspective of the corrective

action program.

In this case.

operability of a containment isolation

valve was adversely affected

by a deficiency related to that cited in an

NRC Notice of Violation several

months earlier.

This was difficult to

detect since the

PER was closed to the

WR as permitted

by the corrective

action program and only the

WR description described

the causal

factors.

Appendix

C of SSP-3.4,

Corrective Action Program.

sets forth criterion

for issues that represent

Level

8 PERs.

The criteria does not

explicitly require

a containment isolation valve failure to be

classified

as

a Level

8 PER..

In response to the inspector's

observations,

Nuclear

Assurance

and management

evaluated

methods to

review effectiveness of corrective actions for

NRC violations.

The inspectors

concluded that overall maintenance

supervision including

painting activities have also been strong in recent months.

No other

issues

involving misapplication of paint have

been identified.

The

violation is closed.

Closed

Licensee

Event

Re ort

LER

260/97-001-00:

Reactor

Scram as

a

Result of Personnel

Error During Surveillance

Testing.

This event

was

discussed

in IR 97-05.

Inspection Follow-up Item 260/97-05-04 'purious

Main Steam Isolation Valve Closure

on Turbine Trip. was opened to review

high steam flow instrumentation

issues.

Violation 260 '96/97-05-02,

Failure to Implement Maintenance

Procedures.

was issued

and addressed

the personnel

error which initiated the event.

No new issues

were

identified in -the LER.

This

LER is closed.

~ 4

25

III. En ineerin

Conduct of Engineering

10 CFR 50.59 Safet

Evaluation Pro

ram

Ins ection Sco

e

37001

The inspectors

performed

a programmatic

review of the licensee's

10 CFR 50.59 procedures

and training requirements

in order to verify compliance

with the regulations

and regulatory commitments.

An evaluation of the

licensee's

performance

in implementing the requirements of Section 50.59

was also performed to assess

the licensee's

resolution of safety issues

related to change.

tests or experiments.

Observations

and Findin s

Procedure

SPP-9.4,

10 CFR 50.59 Evaluations of Changes,

Tests

and

Experiments,

Revision

0

~ established

requirements for review and

evaluation of changes

as required

by 10 CFR 50.59.

The requirements

specified included performing; 1)

a nuclear safety test or Safety

Assessment

and 2)

a licensing test or screening

review and safety

evaluation.

The procedure

assigned

responsibility to line managers

for

assigning qualified preparers

and reviewers for performing safety

assessments,

screening

reviews.

and safety evaluations

consistent with

the complexity and scope of the proposed activity.

Section 3.3,

Qualification and Training of Personnel.

further assigned responsibility

to the Manager of Nuclear Training for administering the

10 CFR 50.59

training program and identified personnel

who are required to be

trained.

The inspector

reviewed lesson plan

EGT 024.007, Qualified 50.59 Preparer

Training,

and determined that it provided specialized

engineering

training in preparing

10 CFR 50.59 Safety Evaluations.

The inspector

also reviewed the "Nuclear Employee Training System

(NETS)

-

LCG 1064.

50.59 Preparer List" dated

March 23,

1998,

and chose

a random selection

of nineteen

10 CFR 50.59 Qualified Reviewers.

These persons

selected

were verified to have completed the training course

requirements.

Based

on objective evidence

reviewed the inspector

concluded that the

Qualified 50.59 Preparer Training met ANSI-3. 1-1981,

concerning

maintaining minimum qualification in operating

and support organizations

appropriate for safe

and efficient operation of Browns Ferry.

Technical Specification

(TS) Section 6.5. 1.6.f assigns

responsibility to

the Plant Operations

Review Committee

(PORC) for review of safety

evaluations

completed

under the provisions of 10 CFR 50.59.

This

responsibility

has

been delegated to the Nuclear Safety Review board

(NSRB)

- Safety Assessment/Safety

Evaluation Subcommittee.

The

NSRB has

identified deficiencies with safety assessments

and safety evaluations

during their reviews.

Because of these recurring problems

an

NSRB

Report Briefing was prepared to bring these

problems to the attention of

all Qualified 50.59 Preparers.

The briefing package

contained

a summary

26

of problems identified by the

NSRB in addition to problems identified by

other reviewers.

Information contained in the briefing package

was used

as lessons

learned in order to facilitate improving performance

in

preparation

and review of 10 CFR 50.59 safety evaluations.

Based

on

objective evidence

reviewed the inspector

concluded,

that the licensee

has

used lessons

learned

and taken actions for improving the preparation

of 10 CFR 50.59 Safety Evaluations.

The inspector

reviewed six 10 CFR 50.59 safety evaluations

chosen at

random from the licensee'.s

1997 Annual Operating Report submittal.

Five

safety evaluations

were determined to be technically adequate

and

demonstrated

consistency

between the design

changes

and information in

the

UFSAR.

The safety evaluation prepared for plant modifications

DCN

No. T30200A,

was identified as being deficient, in that the

SER

incorrectly stated the scope to include the changes to FSAR Table 7.8-2.

Plant modification

OCN No. T30200A, "Issue Unit 2 and

Common Syst'm

NESSDs,"

was approved

on April 28,

1994, in order to issue Unit 2 and

common Nuclear Engineering Setpoint

and Scaling

Documents

(NESSOs).

The

scope of the plant modification stated that the

NESSDs were revised to

reflect minor changes

in their parent calculations.

The total

number of

NESSDs within the scope of the design

change notice also included

NESSDs

that were associated

with earlier issued

DCNs and

NESSDs that were

required for Units 3 restart.

An attachment

"A" to the plant

modifications package

gave detailed information concerning

what had been

changed

by the

NESSDs including implementation

requi rements.

Safety Evaluation

No.

SER

FDCN 940015 Revision 0. dated

June

14,

1994,

was prepared for design

change notice

OCN no.

T30200A.

This safety

evaluation stated that the setpoint

and scaling

changes

issued with the

DCN impacted

FSAR Table 7.8-2.

Based

on review of the safety evaluation

the inspector determined that the following Regulatory Guide 1.97 Post

Accident Monitoring instruments

were impacted.

~

Orywell Pressure

Indication/Recorder

~

Drywell Temperature

Indication

Orywell Temperature

Recorder

~

Suppression

Chamber Water Level Indication (Narrow/Wide Range)

~

Post-accident

Containment

High Level Radiation

Recorder

~

Hydrogen Analyzer

(PAM) Oxygen Analyze

(Normal/PAM).

.

Suppression

Chamber Water Temperature

Indication

FSAR Table 7.8-2.

sheets

1 and

2 was revised to show the range

column of

the as-installed

instrumentation.

Additionally. the Set Trip Point

column was revised to remove the alarm setpoint

values. of the various

instruments

and describe only the trip functions.

Based

on review of-

27

Safety Evaluation

No.

SER

FDCN 940015:

the inspector

determined that

an

evaluation of the changes

to the instruments

ranges

against the

requirements of Regulatory Guide 1.97 had not been performed

by this

SER.

Additionally, review of the instrument loops listed on Attachment

"A" of the design

change notice revealed that the Post-accident

'onitoring instruments

were not within the scope

DCN No. T30200A.

On April 24.

1998,

TVA licensing was informed that objective evidence

indicated that the installation of PAM instruments

and subsequent

changes

to the

UFSAR were accomplished

by a plant modification other

than

DCN No. T30200A.

Pending

NRC review of the other design

change

notice and

10 CFR 50.59 safety evaluation this is identified as IFI 50-

260,296/98-02-06.

Review

DCN and Safety Evaluation for FSAR Table 7.8-2

Changes.

Conclusions

The inspector

concluded that the licensee's

gualified 50.59 Preparer

Training met ANSI-3. 1-1981.

concerning maintaining minimum qualification

in operating

and support organizations

appropriate

for 'safe

and

efficient operation of Browns Ferry.

The licensee

has

used lessons

learned

and taken actions

for improving the preparation of 10 CFR 50.59

Safety Evaluations.

Of the six 10 CFR 50.59 safety evaluations

chosen

for review, five were determined to be technically adequate

and

demonstrated

consistency

between the design

changes

and information in

the

UFSAR.

One safety evaluation

had

a minor deficiency, in that the

SER incorrectly stated the scope of the change.

IV. Plant

Su

ort

Radiological Protection

and Chemistry

(RP8C) Controls

Postin

of Notices to Workers

Ins ection

Sco

e

71750

A resident

inspector

reviewed the licensee's

posting of notices to

workers requi red by 10 CFR 19. 11.

Observations

and Findin s

The inspector verified that the required notices

were posted at all

security checkpoints to the protected

area.

The Materials Procurement

Center

and the Administration Building located outside the protected

area

were also checked.

The inspector

found that

some of the required

information was not posted at these locations.'owever,

as allowed by

10 CFR 19. 11, the licensee

posted

a notice that described

the documents

and stated that the documents

were available to be inspected

in the

Technical

Information Center.

The inspector verified that the required

documents

were available in the

Technical

Information Centers

The inspector interviewed Technical

~ y,

28

Information Center

personnel

and found them to be knowledgeable of the

documents

and their locations (e.g..

operating license

and amendments,

code of federal regulations).

c.

Conclusions

The licensee properly'osted, required notices to workers

as required

by

10 CFR 19. 11.

Technical

Information Center personnel

were knowledgeable

of the locations of documents

required to be available to workers.

V. Hang ement Meetin s

X1

Exit Heeting Summary

The resident

inspector

presented

inspection findings and results to

licensee

management

on April 20,

1998.

The licensee

provided

some

dissenting

comments

regarding the issue in Section H1.2.

The licensee

stated that the

ASHE code requirements

had been met for inspection of

the rupture disc.

Other meetings to discuss

report issues

were

conducted during the report period including formal meetings with plant

management

on March 6 and April 3.

1998.

Subsequently,

additional

discussion of the issues

in Section 05. 1 were discussed

by telephone

with the inspector

and regional

management.

The licensee

acknowledged

the findings presented.

Proprietary information is not included in this

inspection report.

PARTIAL LIST OF PERSONS

CONTACTED

Licensee

T. Abney, Licensing Manager

J. Brazell, Site Security Manager

R. Casey.

Manager.

Access Authorization/Fitness for Duty

R. Champion,

Operations Training Manager

R. Coleman, Acting Radiological Control Manager

J.

Corey, Radiological Controls

and Chemistry Manager

C. Crane, Site Vice President,

Browns Ferry

R. Greenman,

Training Manager

J.

Johnson.

Site Quality Assurance

Manager

R. Jones.

Assistant Plant Manager

R. Moll. System Engineering

Manager

G. Little. Operations

Manager

D. Nye, Site Engineering

Manager

D. Olive. Operations

Superintendent

J.

Shaw,

Design Engineering

Manager

K. Singer,

Plant Manager

J. Schlessel,

Maintenance

Manager

IP 37001:

IP 37551:

IP 40500:

IP 62707:

IP 61726:

IP 71001:

IP 71707:

IP 71750:

IP 73756:

IP 81502:

IP 82701:

IP 83750:

IP 84750:

IP 86750:

IP 92901:

IP 92902:

IP 92903:

IP 93702:

29

INSPECTION PROCEDURES

USED

10 CFR 50.59 Safety Evaluation

Program

Onsite Engineering

Licensee

Self-Assessments

Maintenance

Observations

Surveillance

Observations

Licensed Operator Requalification

Program Evaluation

Plant Operations

Plant Support Activities

Inservice Testing of Pumps

and Valves

Fitness

For Duty Program

Operational

Status of the Emergency

Preparedness

Program

Occupational

Radiation

Exposure

Radioactive

Waste Treatment.

and Effluent and Environmental

Monitoring

Solid Radioactive

Waste

Management

and Transportation

Of

Radioactive Materials

Follow-up-Plant Operations

Follow-up-Maintenance

Follow-up-Engineering

Prompt Onsite

Response to Events

ITEMS OPENED

DISCUSSED

AND CLOSED

OPENED

~T

e

Item Number

Status

VIO

259,260,296/98-02-01

Open

VIO

259,260,296/98-02-02

Open

VIO

259,260,296/98-02-03

Open

Descri tion and Reference

Failure to meet minimum shift crew

requirements

(Section 05. 1).

Failure to Follow High Efficiency

Particulate Air Filter Testing

Procedures

(Section Hl.1).

Inadequate

Testing of Downstream

Standby

Gas Treatment

HEPA Filter

(Section Hl.l) .

VIO

260/98-02-04

IFI

260,296/98-02-05

IFI

260, 296/98-02-06

Open

Open

Open

Failure to Identify Degraded

HPCI

Rupture Discs (Section H1.2).

Use of Personnel

in Place of

Equipment Clearances

(Section M1.3).

Review

DCN and Safety Evaluation for

FSAR Table 7.8-Z Changes

(EA No. 98-

241) (Section E1.1).

CLOSED

~T

e

Item Number

LER 296/97-005-00

LER

260/97-004-00

LER 260/97-008-00

LER

296/97-003-00

VIO

260. 296/96-10-02

LER 260/97-001-00

Status

Closed

Closed

Closed

Closed

Closed

Closed

30

Descri tion and Reference

When

a Valve was Malfunctioning'n

LCO was not Entered

(Section 08. 1).

Technical

Speci fi cation

Suryeillances

Were Not Performed

During Refueling Outage

Time frames

(Section M8.1).

Main Steam Safety Valves Exceeded

Technical Specification

(TS)

Required Setpoint Limit as

a Result

of Pilot Valve Disc/Seat

Bonding

(Section H8.2).

Hain Steam Safety Valves Exceeded

Technical Specification

(TS)

Required Setpoint Limit as

a Result

of Disc/Seat

Bonding (Section M8.2).

Inadequate

Supervisory Oversight of

EDG Painting Activities (Section

M8.3).

Reactor

Scram as

a Result of

Personnel

Error During Surveillance

Testing (Section H8.4).

ig