ML18038B815

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Insp Repts 50-259/96-13,50-260/96-13 & 50-296/96-13 on 961124-970104.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support
ML18038B815
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 01/27/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18038B813 List:
References
50-259-96-13, 50-260-96-13, 50-296-96-13, NUDOCS 9702100334
Download: ML18038B815 (44)


See also: IR 05000259/1996013

Text

-

U.S.

NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

License

Nos:

50-259,

50-260,

50-296

DPR-33',

DRP-52,

DPR-68

Report

No:

50-259/96-13,

50-260/96-13,

50-296/96-13

Licensee:

Tennessee

Valley Authority (TVA)

Facility:

Browns Ferry Nuclear Plant, Units 1, 2,

and 3

Location:

Corner of Shaw and Browns Ferry Roads

Athens,

AL

35611

Dates:

November 24,

1996

- January 4,

1997

Inspectors:

Approved, by:

H. Morgan, Acting Senior

Resident

Inspector

.J. Starefos,

Resident

Inspector

G. Walton, Reactor Engineer

(Paragraph

E8.2)

H. 'Lesser,:Chief

Reactor Projects

Branch '6

'.Division of 'Reactor 'Projects

Enclosure

2

9702i00334 970127

PDR

ADOCK 05000259

8

'PDR

41

Cb

EXECUTIVE SUMMARY

Browns Ferry Nuclear Plant, Units 1,

2

8 3

NRC Inspection Report 50-259/96-13,

50-260/96-13,

50-296/96-13

This integrated inspection included aspects of licensee operations,

engineering,

maintenance,

and plant support.

The report covers

a six-week

period of resident inspection

and includes efforts of a regional

reactor

engineer.

0 erations

On December

17.

1996. the 2A Battery Charger

was aligned to restore g2

Hain Battery Bank voltage levels.

The charger would not build-up to

adequate

levels

and was taken out of service.

However,

when the 2B

charger

was used it gave fluctuating amps.

The licensee properly

addressed

and repaired both char gers.

(Section 02.1).

~

On December

17,

1996, the Unit 3 Division II ECCS Inverter power

was

lost due to a fuse failure.

Repairs

were immediately performed,

the

fuse was replaced,

inverter was tested

and placed back into service.

An

ECCS backup supply is scheduled for installation during the Unit 3

outage.

The cause of the inver ter failure was not fully determined.

Inspection Followup Item 296/96-.08-02

discussed

recurring failures of

inverters

and remains

open.

(Section 02.2).

On, December

13,

1996, Unit 3 Operations

experienced

an unplanned,

ar tial

ESF actuation

when an external

120VAC power supply tripped

a

reaker during adjustment of a continuous air monitoring valve limit

switch.

Immediate corrective actions by the licensee

were adequate.

~(Section 02.3).

\\

During the inspection period, the inspectors

reviewed

a licensee

proposal to use Auxiliary Unit Operators

(AUOs) and Site Secur ity

personnel, as. Fire Watches.

The inspectors

found that the use of AUOs

and .Site Security as Fire Watches

was acceptable.

(Section 06.1).

Maintenance

Continued. review of fr eeze protection program activities found that

licensee efforts were adequate to provide necessary

protection.

(Section

H1'.1) .

The inspectors

reviewed licensee

Toolpouch Maintenance efforts.

The

inspectors specifically addressed

use of this Toolpouch Maintenance for

Emergency Diesel

Gener ator

per iodic maintenance.

The inspector s

I!

0

-questioned

the appropriateness

of applying Toolpouch to a Diesel

Generator activity and identified

a potential for adding incorrect

chemicals.

Unresolved Item,

URI 50-259,260,296/96-13-2

was opened.

(Section H1.2) .

~

On December

12,

1996 during

a refuel area tour the inspectors

noted that

a tarpaulin-type cover was erected

over the Unit 2 Spent

Fuel

Pool

(SFP).- The inspectors

found that maintenance

personnel

had failed to

properly implement work control procedures

and thus

an evaluation of

impact on SFP design

and operation

was not performed.

A violation (VIO)

50-260/96-13-01

was identified. (Section H2.1).

~

On November 27,

1996, during a licensee

inspection of Unit 3 SFP cooling

system,

a rag was found in check valve 3-CKV-'078-0545.

On December 4,

1996, prior to eddy current testing,

during an examination of the 2A SFP

cooler

head assembly,

workers found three pieces of non magnetic metal

and

a piece of wire.

All items were analyzed

and determined to have

entered the systems

during outage or construction activities.

The

inspectors

noted that licensee

response to the problem was very good.

~(Section H2.2).

En ineerin

On November 21,

1996, licensee

Reactor Engineering personnel

were

informed by the reactor fuel vendor that there was

a potential input

error in analysis

performed for the Unit 3 Average Planar Linear Heat

Generation

Rate

(APLHGR) which, in turn,

made the APLHGR limits

nonconser vative.

.In a follow-up January,

1997 vendor letter, the vendor

reassessed

the APLHGR calculations

and determined that they had not

calculated

an allowance for fuel pellet densification

effects.'eperformed

calculations

wer e conservative.

Inspector s noted that the

l,icensee

responded

appropriately to these notifications.

(Section E2.1).

During the inspection period, the inspectors

reviewed hourly regular

time and overtime hours for licensee

system/technical

engineering

and

radiological control personnel.

The inspectors

found that personnel

in

these work groups worked very little overtime and hours were well within

times allotted for in .Site Standard Practice procedure

SSP-1.7,

Overtime

Restrictions

- 'Regulatory.

(Section E6.1).

During the inspection period, .the inspectors

noted that twenty-eight

fuse program corrective action items had been presented

in 1996.

After

further review the inspectors

concluded that the high number of issues

was due to a combination of a new initiative f'r field identification of

.fuses

and

a low. threshold for reporting problems including non safety-

related equipment.

(Section E8.1).

Ib

0

0

-J

~

On December

27,

1996, the licensee identified an .uncontrolled -Locked

High Radiation area.

While the area

was unlocked, AUOs/electrical

maintenance

personnel

entered the area

and received unanticipated

exposures.

The inspectors identified two examples of inadequate

procedures

which contributed to the event

and

a violation (VIO) 50-

296/96-13-3

was identified. (Section Rl.l).

0

il

0

R~R

Summar

of Plant Status

Unit 1 remained in a long-term lay-up condition with the reactor defueled.

With the exception of a December

26,

1996,

power reduction to clean unit main

condenser

waterboxes,

Unit 2 operated

at power during the report period.

Also, with the exception of .the periods noted in the following paragraph,

Unit 3 continued its planned

coastdown

as the Unit 3 Cycle 7 outage

approached.

On November 29,

1996,

December

27,

1996,

and January 3,

1997, Unit 3 power was

reduced

from approximately 95'ower to 70'ower

and then returned to highest

allowable power conditions.

These

power variations were performed to adjust

feedwater

heater configurations.

These feedwater

heater configuration changes

were performed to adjust feedwater temperatures

during thy unit coastdown for

the February 21,

1997, Unit 3 Cycle 7 refueling outage.

I.

rations

02

Operational

Status of Facilities and Equipment

~

~

02.1

Unit 2 Batter

Char er Failures

a.

Ins ection Sco

e

71707

92700

93702-

The inspectors

reviewed the actions taken by the licensee in response to

2A and

2B Battery Charger

Failures.

b.

Observations

and Findin s

On December

17,

1996, while the Unit 2 2A charger

was aligned to restore

the g2 250VDC Hain Battery Bank from a battery discharge test, the

battery would not build-up enough charge nor indicate adequate

voltage

levels.

The 2B charger

(the spare)

was then aligned to the bank.

However,

on December

18,

1996, at .1:00 a.m.,

(CST), after approximately

3 hour3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> s of oper ation, this charger displayed fluctuating amper ages.

This portion, of the battery equalizing charge surveillance

was

immediately secured

and the 2B charger

was removed from service for

troubleshooting

and repairs.

The unavailability of the 2A and

2B chargers

presented

a loss of both

Hain Battery Bank $2 power supplies,

and the licensee

enter ed

a 24-hour

Technical Specification

(TS) Limiting Condition for Oper ation

(LCO)

3.9.B.7,

Loss of a Shared

Source of DC Power .

Two other sources of DC

power

(the Unit 2 g3 and g4 char gers),

and three other battery banks

were available throughout testing

and this .event.

Troubleshooting efforts determined the 2B charger

amperage oscillations

were caused

by a failed resistor.

The resistor

was replaced,

the

charger

was tested,

and at about 1:00 p.m.

(CST) on December.

18,

1996,

Ci

0

I

the charger

was 'returned to service.

Unit 2 Hain Battery Bank

survei1lance testing

was then completed.

During rep1acement

of the resistor; the inspector

observed that. craft

personnel

were attentive to their repair activities.

They had noted

that the replacement

resistor required suitable

and appropriate

dedication prior to use in the charger

because this resistor could no

longer be purchased

nor obtained

as

a safety item.

Additionally, a

capacitor

was replaced in the 2A charger.

Licensee-approved

component

dedication activities were performed in a satisfactory

manner,

the

resistor

was properly qualified for use,

and repairs were performed.

Conclusions

The inspectors

determined that the licensee properly addressed

the

failures and subsequent

unavailability of both chargers.

Licensee

notification of the event

was both timely and accurate.

Although

evidence of the problem was almost negligible (variations in amperage

initially observed

by the craft were slight)

a call for repair was

immediately made

and subsequent

charger troubleshooting

and repair

efforts were quickly performed.

Unit 3 Emer enc

Core Coolin

S stem

ECCS

Division II Inverter Failure

Ins ection Sco

e

71707

92700

93702

The inspectors

reviewed actions taken by the licensee in response to a

Unit 3 Division II ECCS ATU Inver ter power failure.

Observations

and Findin s

On December

17,

1996, Unit 3 Division II ECCS ATU Inverter

power

was

lost due to a fuse failure.

This inverter supplies

power to two of four

channels of drywell pressure

and the reactor water level sensors.

These

sensors

supply both divisions of initiation logic for RHR/CS,

HPCI, ADS,

and the

EDGs.

Other sensors for reactor pressure,

containment

and HPCI

are also supplied by this inver ter

.

Because the other channels of ECCS instrumentation

are powered by the

Division I inverter, the logic of all

ECCS divisions would have been

initiated, if required.

With the exception of HPCI and Division II

input into the Anticipated Transient Without Scram

(AVOWS)/Recirculation

Pump Trip (RPT) logic, all systems

would have performed their design

function.

Because this ATWS/RPT logic was inoperable,

a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />

LCO (TS 3.2.L) .was entered.

The Division I ATWS/RPT logic was operable

and

would have performed

as designed.

Approximately two and one-half hours after the inverter was lost, the

fuse was replaced

and other circuitry items; i.e., the SCR/Diode,

control board

and capacitor;

were checked in accordance

with work order

(WO) 95-022182-001.

The inverter was subsequently

tested

and performed

4l

0

C.

02.3

a.

b.

'atisfactorily.

The

LCO was exited and the inverter was placed

back in

service:

All ECCS systems

were restored to pre-event conditions.

There have been other recent Unit 3

ECCS Division I inverter failures

(See

IR 96-08, Section 02.2 and IR 96-12, Section 02.2).

A descr iption

of these Division I failures is presented

in Unit 3 LER 296/96-004,

Revision 2 and Unit 3 LER 296/96-006.

The licensee

has issued Unit 3

LER 296/96-008 to describe this Division II inverter failure.

Conclusions

A licensee analysis to determine the exact cause of both the Division I

and II inverter failures is on-going.

The licensee is implementing

a

backup source of uninter ruptable

("DC-to-DC") power to the Division I

and Division II circuitry.

The inspectors

have reviewed

DCN T39853A;

which documents installation of this power supply modification in the

upcoming February

1997 Unit 3 refueling outage.

The inspector s

determined that the licensee's

actions are appropriate

and this backup

source of logic power will mitigate the effect of similar failures.

Because

a specific cause of the Unit 3 Division I and II failures have

.not yet been determined

by the licensee (test results are expected in

late February

and ear ly Harch) the issues will remain open

and continue

to be addr essed in Unit 3 Inspection Followup Item (IFI) 296/96-08-02,

Emergency Core Cooling System Inverter Failures.

Un lanned Unit 3

H dro en/Ox

en Anal zer Valve Isolation

Ins ection Sco

e

71707

92700

93702

The inspectots

reviewed actions taken by the licensee in response to an

unanticipated partial Unit 3 Engineered Safety Features

(ESF) Actuation

and

a subsequent

inadvertent isolation of the Hydrogen/Oxygen

(H,O,)

analyzers.

Observations

and Findin s

On December

13,

1996, Unit 3 operations

experienced

an unplanned,

partial-ESF actuation

when adjustment of a limit switch for continuous

air monitoring valve (FSV-84-8D) caused

an external

120VAC power supply

Iinstrumentation

and control

(I8C) panel g9-9] breaker

f336 to trip.

During these

adjustment activities, the primary containment isolation

system

(PCIS) breaker

f336 opened,

which deenergized

PCIS valves

and

positioned the

Hz0 valves to their fail safe position (both divisions

oi'he drywall anrf torus

H,O, sample/return line valves closed).

Operators took proper

immediate actions in response to the isolation and

the unit continued at full power operation throughout the event.

Because

both divisions of the

H,O> analyzers

were isolated,

Technical

Specification

(TS) Limiting Condition for Oper ation

(LCO) 3.7.H.3 was

entered

which required the licensee to have the reactor

in Hot Shutdown

in 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

Licensee Operations

determined that the root cause of'he

0

event

was weak planning of a step-text

work order

(WO).

During work

planning activities,

WO steps

were not sequenced

in accordance

with

expected activity practices.

The tripped panel

breaker

was immediately

reset,

the

H,O, analyzer valves were reopened,

and the

LCO was exited.

c.

Conclusions

The inspectors

determined that the work planning did not meet the

licensee's

expectations

and corrective actions were appropriate.

The

inspectors,

Region II, and

NRC Headquarters

personnel

were promptly

notified'f the partial-ESF actuation.

A licensee

event report

(LER 96-

007-00)

was submitted in accordance

with 10 CFR 50.73(a)(2)(iv).

06

Operations Organization

and Administration (71707)

06. 1

Use of Auxiliar Unit 0 erators

AUO

and Securit

Staff as Fire Watches

a.

Ins ection Sco

e

71707

64704

The inspectors

reviewed licensee

plans to use

AUOs and Security

personnel

as Fire Watches to determine if these

proposed activities

would be performed in accordance

with guidance contained in SSP-12.1,

Conduct of Operations,

Revision 30; the Site Security Plan;

and Licensee

Fire Protection Report

(FPR), Section I-L, Revision 2.

b.

Observations

and Findin s

The inspectors

reviewed

a licensee

plan to use

AUOs and Site Security

personnel

as Fire Watches.

The plan. indicated that AUOs would be used

as Roving Fire Watches

and that in this capacity the

AUO would have no

other duties which impacted their fire watch function.

The plan also

indicated that extra AUOs, those not assigned to perform standard

AUO

duties,

would be tasked

by the Shift Hanager to perform Roving Fire

Watch functions.

The inspectors

determined that the licensee's

program has the following

requirements:

Fire watch personnel

must have training in performance of the

Roving Fire Watch function and use of FP equipment.

A documented

record of such, training must be available/accessible.

AUO personnel

performing .the Roving Fire Watch function must

accomplish their assigned

Roving Fire Watch tasks

and log/record

FP task completion within the

FPR designated/approved

time frames.

Any personnel

performing the function of a Roving Fire Watch must

not have any other responsibilities

which could have

an impact

upon their assigned fire watch duties.

0

C.

08

08.1

The inspectors,

during their review of the licensee's

proposal,

noted

a

potential conflict in responsibilities

as delineated in SSP-12.1

and the

FPR.

According to SSP-12.1,

an

operator 's primary responsibility is the

proper

and safe operation of the plant, whereas,

according the

FPR, the

fire watch has

a primary responsibility of watching for and responding

to fires or potential fire hazards.

This apparent difference in basic

watchstanding responsibilities

was brought to the attention of the Fire

Protection

and Operations

Hanagement.

The inspectors

understand that

.clarification of AUO/Roving Fire Watch responsibilities,

in the form of

a SSP-12.1 revision, is on-going and is planned for completion in

February or Harch,

1997.

The inspectors

also reviewed

a licensee

proposal to use Site Security

personnel

as Continuous Fire Watches whi'le they are also being used to

control access

to normally closed/locked vital areas.

The inspectors

discussed this with licensee

management

and noted that the licensee

intended to use posted

guards in the following manner:

~

Site Security personnel

are to stay on station

and at their

assigned

posts.

~

On-Station Site Security personnel's

only actual fire watch

function is maintaining awareness

of actual or potential fire

hazards.

~

If personnel

are unable to view all zones

from the open door area,

they must request

assistance

to perform the fire watch function.

~

If an actual

hazard exists, Site Security will immediately;

1)

inform personnel

in the area being watched to evacuate,

2) close

the door to the area,

and 3) call for fire brigade assistance.

The inspectors

also noted that the three previously specified Fire Watch

~ requir ements for the AUOs are also required for Site Security personnel

performing the Continuous Fire Watch function.

Conclusions

The inspectors

found that the licensee's

plan to use

AUOs as Roving Fire

Watches

and Site Security personnel

as Continuous Fire Matches (while

such personnel

are stationed at their assigned

security posts)

.was

acceptable.

The inspectors

also found that the planned February/Harch

1997 revision to SSP-12.1,

to be performed in or der to clarify AUO

Roving Fire Watch responsibilities,

once implemented, will be

acceptable.

Hiscellaneous

Operations

Issues

(92901)

(Closed)

LER 50-296/96-004:

Unplanned

ESF Actuation Following Transfer

of 480VAC Shutdown Board 3A To Its Alternate Supply.

This

LER was

submitted

due to an event .that resulted in an automatic actuation: of

ESF.

After a licensed operator

had mistakenly transferred the 3A 480VAC

P

0

i~

Shutdown Board power .from an energized

source of power to a'eenergized

power

source

a half-scram

was received

on Reactor Protection

System

(RPS)

Bus 3A.

This action, in turn, initiated an

ESF signal

and the

unit then experienced

an inadvertent

and unexpected

actuation of the

standby gas treatment

system

(SGTS), the control

room emergency

ventilation system

(CREVS),

and the primary containment isolation system

(PCIS).

The root cause

was determined to be personnel

er ror.

Based

upon the inspector-observed

satisfactory completion of the licensee's

immediate corrective actions

and tHe completed corrective actions

designed to prevent recurrence,

this

LER is closed.

Conduct of Maintenance

II. Maintenance

Continued Ins ection of the Licensee's

Freeze Protection

Pro ram

Ins ection Sco

e

71714

92902

The inspectors

continued to review activities related to the licensee's

freeze .protection program

(See IR96-12, Section

H8 ~ 2) to determine if

activities were conducted in accordance

with BFN procedure

0-GOI-200-1

Freeze Protection Inspection,

Revision 25 and

WO $96009582000,

Annual

Inspection

and Preventative

Maintenance of Freeze Protection

Systems.

Observations

and Findin s

From December

16 to December

20,

1996, the inspectors

toured various

plant areas,

(specifically, the condensate,

demineralized

water

and

chemical

storage tank areas),

and continued

an on-going inspection of

licensee

freeze protection activities.

Many of the inspector -identified

items involved minor discrepancies

(i.e., inadequately lubricated valves

and missing .screws

on var ious heat trace

compartment

doors)

and these

items were immediately brought to the attention of licensee

management

personnel.

The inspectors

also noted that heat tracing thermostat

adjustment

covers (for the condensate

storage

tank and the demineralized

water tank thermostats)

had been left open after

adjustments to the

thermostats

were made by BFN'lectrical Maintenance

(EH) personnel.

By

EH personnel

leaving the covers

open, the thermostat internals were

exposed to various environmental effects

such

as moisture,

cold

temperatures,

and rain/ice conditions.

Such conditions could have

affected designed tank thermostat operation.

This issue

was also

immediately reported to EH supervisory personnel

and licensee

management.

When low temperature

conditions (less than 25 degrees

F) were reached,

the inspector s toured tank and circulating water/RHRSW intake areas

and

noted that appropriate

heat trace lighting, indications were present.

The inspectors

also verified proper heat tracing measurements

(circuitry

ohm measurements)

during a review of BFN Freeze Protection documentation

0

4l

~O

EP I-0-000- FRZ003,

Fr eeze Protecti on Progr am for Miscellaneous

Yard Areas

Buildings and Systems.

c.

Conclusions

Licensee efforts were effective and identified several

issues (i.e.

a

grounding problem with ¹5 condensate

storage tank heat trace).

Continued inspector review of licensee

freeze protection procedures

and

on-going

BFN freeze protection program field activities revealed that

current licensee efforts are adequate

to provide necessary

protection to

guard against cold weather conditions in the area.

H1.2

Use of Tool ouch Maintenance for EDG Maintenance

a.

Ins ection Sco

e

62707

The inspectors .reviewed aspects of Toolpouch Haintenance

on the

emergency diesel

generators

and aspects of the process for ensuring

correct chemistry in the jacket water cooling system.

The inspector s

reviewed the records

and Information Management

computer system

(RIHS);

reviewed SSP-6.2,

Maintenance

Management

System,

Revision 21,

Appendix T, Implementing Toolpouch Maintenance;

reviewed Integrated

TVA

Materials System data;

examined

Power Stores Transaction

System data;

reviewed Chemistry Instruction CI-628.

NALCO-39 (Rust Inhibitor),

Revision 3; reviewed chemistry data;

and reviewed SSP-13.1,

Chemistry

Program,

Revision 14, Appendix C, Table of Bulk Chemicals

Used at BFN.

b.

Observations

and Findin s

Work Order 96-012915-000

was.reviewed

from the computer tr acking system

(Enterprise-HPAC).

The inspectors

determined that

WO action indicated

that Toolpouch Haintenance

was performed to raise the diesel

coolant

expansion tank level.

The work description stated

"Added demin water to

bring level

up to 9 1/4, about

5 gal" and the

WO status indicated

"complete to document control" (CD).

The inspectors

searched

the RIHS

(Records

and Information Hanagement)

computer system to determine if

documentation

from,the

WO and

Wor k Request

WRNRepair Tag were archived

on microfiche.

No records

were found.

A lack of physical

documentation of the

WO is consistent with closure of

work using Toolpouch Haintenance.

Licensee

procedure

SSP-6.2

Haintenance

Hanagement

System,

Revision 21, Appendix T, states in

associated

notes .that

"No documentation of work activities is required

for work performed

as Toolpouch Haintenance;"

however, the inspectors

questioned

whether

use of Toolpouch Haintenance

was acceptable

for the

work described in the

WO.

The licensee is currently evaluating whether Toolpouch Haintenance

was

appropriate for adding demineralized

water to the emergency diesel

generators

(EDGs) cooling system.

The licensee

has also initiated a

PER

(BFPER961761) to document this evaluation.

Licensee

management

has also

indicated that Toolpouch Haintenance will not be used for the indicated

0'

41

C.

H2

H2.1

a.

example until the licensee

has addressed

this issue.

An Unresolved

Item

will be opened to follow their evaluation

(URI 50-259,260,296/96-13-02).

The .inspectors

questioned if the addition of demineralized

water

affected the coolant chemistry.

During review of Integrated

TVA

Haterials

System data,

the inspectors

determined that

a corrosion

inhibitor (TIIC MANX-359P) and

a liquid antifreeze,

ethylene glycol

(TIIC KBG-732L) could be issued for any of the eight

EDGs.

The

inspectors

questioned

whether the liquid antifreeze

was acceptable

for

use in the

EDGs.

The licensee initiated

PER

(BFPER970056) to address

whether TIIC gCBG-732L (liquid antifreeze)

can be added to the

EDGs

contrary to SSP-13.1.

SSP-13.1,

Chemistry Program,

Revision 14,

Appendix C, Table of Bulk Chemicals

Used at BFN, described the use of

Diesel

Generator

Jacket Cooling Corrosion Inhibitor in the

EDGs.

Ethylene Glycol was not addressed

by SSP-13-1

as acceptable

for use in

the

EDGs.

The inspectors will also address this issue in the Unresolved

Item (URI 50-259,260,296/96-13-02).

The inspectors

also reviewed the

Power

STORES Transaction History for

the issuance of the liquid antifreeze

(TIIC CBG-732L).

The

documentation did not indicate that the liquid antifreeze

had been

issued for use

on an

EDG.

The inspectors

reviewed chemistry data for all eight emergency diesel

generator s from January

1995 through November 1996.

Chemistry

Instruction CI-628,

NALCO-39 (Rust Inhibitor), Revision 3, determines

the concentration of rust inhibitor

(NALCO-39) in the diesel

generator

cooling system.

The procedure

addr esses

the minimum required

concentration

as 2.2 ounces/gal.

Based

upon the data reviewed, the

concentration did not drop below the procedure required concentration of

2.2 ounces/gal.

Conclusions

The inspector will followup on the concerns identified through

Unresolved

Item (URI 50-259,260,296/96-13-02).

Although the possibility

existed for the liquid antifreeze

(TIIC CBG-732L) to be issued for the

Emergency Diesel Generators,

review did not indicate that liquid

antifreeze

has

been

used in the Emergency Diesel Generators.

Haintenance

and:Haterial

Condition of Facilities and Equipment

A

Placement of a Unit 2 S ent Fuel

Pool Cover Without Pro er Work Control

Ins ection Sco

e

62707

92902

The inspectors

examined work control activities associated

with the

placement of a tarpaulin-type cover over the Unit 2 Spent

Fuel

Pool

(SFP) to determined if they were conducted in accordance

with licensee-

approved work control practice procedures.

II

~li

b. "Observations

and Findin s

On December

12,

1996, during

a routine tour of the spent fuel pool area,

the inspector s observed that

a tailored, reinforced-plastic,

yellow,

tarpaulin-type,

cover had been erected

over and around the upper

surface

area of the SFP.

The inspector s determined that this cover had

apparently

been placed over the

SFP for FHE purposes.

Upon further

inspection,

the inspectors

discovered that this SFP modification had not

been properly processed

through

a licensee-approved

work control

process.'y

not performing approved work control processes,

this change

to the original

SFP design

was not thoroughly evaluated

by Operations

nor Licensee Engineering for impacts

on SFP operation

and design.

As stated in licensee-approved

procedure

SSP-7.1,

Work Control,

Revision 15, this procedure is to be performed for all activities that

change or have the potential to change

a component,

system or unit

configuration.

Section 3.2.1.A of SSP-7.1

notes that

an initiator of a

work activity is to prepare

a work request for activity performance

and

after review by the initiator's supervisor,, this request is to be

forwarded to Operations for further review.

Operations

review,

according to Section 3.2.1.B of SSP-7.1,

affords unit operations

an

assessment

of potential

impacts of the activity (and related

system

change)

on unit operations.

Operations

and engineering

were not afforded opportunities to assess

the

cover's

impact on the designed operation of the pool.

An engineering

evaluation of the cover's

impact upon original design of the

SFP was not

performed.

The SFP cover's configuration was not evaluated

by licensee

engineering for effects

on designed

SFP heat dissipation,

influence on

designed

SFP ventilation air exchanges

or for any impacts

upon

SFP water

purity, or operational

impacts

and controls such

as fire loading;

inspections -etc.

C.

H2.2

Conclusions

The inspectors

concluded that licensee

maintenance

personnel

failed to

adequately

implement licensee-approved

work control procedures.

By not

implementing these

procedures,

licensee

personnel

failed to provide

BFN

Operations

and Engineering

an opportunity to evaluate the impact of this

cover

on SFP design

and operation prior to installation of the cover.

This issue is identified as Violation (VIO) 50-260/96-13-01,

Failure to

Implement Licensee-Approved

Work Controls for Changes to the SFP.

Forei

n Haterial

'Exclusion

FHE

Issues

a.

Ins ection Sco

e

62707

92902

The inspectors

examined activities associated

with the discovery and

subsequent

removal of a rag located in a Unit 3 SFP cooling system check

valve (3-CKY-078-0545).

The inspectors

also reviewed licensee

discovery

and subsequent

licensee

removal activities involving three pieces of

0

10

non-magnetic

metal

and

a piece of wire found in the inlet/outlet head

area of the Unit 2 cooler/heat

exchanger

(2-HEX-78-758).

Observations

and Findin s

On November 27,

1996, during

a licensee

inspection of SFP cooling system

check valve 3-CKV-078-0545,

a rag was found in the valve.

Plant

maintenance

personnel

removed the rag during performance of WO 95-03507-

00 (as

par t of the licensee's

on-going safety system check valve

inspection efforts)

and sent it to their laboratory for analysis.

Based

upon actual

appear ance .and condition of the rag fibers, the rag was in

the system we)l before the 1995 Unit 3 restart/recovery

peri'od.

The

licensee further presumed that the rag may have hooked itself upon

system

component internals

and/or piping during past system flushing

efforts.

Because of this hooking action, the rag was, therefore,

not

expelled .from the piping as expected.

They also determined,

by lack

of'ignificant

variance

from expected

flow during system operation, that

the rag did not affect check valve operability.

On December

4,

1996, prior to performance of a preventive maintenance

inspection

and eddy current testing of the 2A SFP Cooler (2-HEX-78-758)

three pieces of metal

(squares of about 3/4 inch

X 1/4 inch)

and

a piece

of what appeared to be bailing wire (approximately

3 inches long) was

removed from the inlet/outlet head of the cooler.

After removal this

material/debris

was sent to the licensee's

corporate

laboratory for

analysis in order to determine material

makeup

and origin.

The licensee

determined that the squares

were non-magnetic

and appeared

to be pieces of a tool or possible

shim pieces.

The wire was that of a

type used .to tie-off scaffolding.

The licensee

presumed that the metal

squares

and the wire entered the

SFP heat exchanger

head area during

revious maintenance

on the

SFP cooler/heat

exchanger

and probably had

een in the head area for greater than 2 years.

Conclusions

The inspectors

noted that licensee

maintenance

personnel

had properly

prepared for the possibility of having foreign material in the cooler

upon initially opening

up the head for eddy current testing.

Personnel

were very good in finding this material,

and they were also very prompt

and thorough in their follow-up analysis.

The licensee

also was

thorough in their analysis of the rag and their determination of source.

The inspector s determined that the licensee's

actions in response to

discovery of this foreign material in each instance

was appropriate.

E2.1

a.

b.

C.

11

III. En ineerin

Engineering Support of Facilities and Equipment

Vendor's

Fuel Calculations for Unit 3

Ins ection Sco

e

37551

The inspectors

examined licensee activities related to the discovery of

what the licensee's

fuel vendor initially thought was

a non-conservative

calculation of the Average Planar Linear Heat Generation

Rate

(APLHGR).

Observations

and Findin s

On November

21,

1996, licensee

Reactor Engineering personnel

were

notified by the fuel vendor of a potential

input error in the Loss of

Coolant Accident

(LOCA) analysis

performed for the Unit 3, Cycle 7 fuel.

The licensee's

fuel vendor initially thought that. their error might have

resulted in non-conservative

APLHGR limits for some of the licensee's

long-lived fuel designs; i.e., the latest version vendor fuel used in

mixed fuel configurations.

The vendor initially estimated that this

error could have resulted in a non-conservative limit error of up to

three percent.

The licensee's

Reactor

Engineering group reviewed the

calculations for Unit 3, Cycle 7 to determine if ther e were any

instances

where limits could have been exceeded.

They determined that

relevant limits had not been

exceeded

throughout the operating cycle.

In a follow-up January,1997

vendor letter to the licensee,

the vendor

stated that they had re-analyzed their November calculations

and noted

that they had not adequately

adjusted the previous

November calculations

to account for (allow for) fuel pellet densification

as the fuel was

operated

throughout the cycle.

By factoring in this item, the original

conservative limit.estimates for APLHGR proved to be just as valid and

just as conservative

as originally designed

and calculated.

Conclusions

The inspectors'noted

that the l,icensee's

Reactor

Engineering/Hanagement

ersonnel

had responded

appropriately to the initial vendor notification

y immediate (historical) verification that

APLHGR limits had not been

exceeded

during operation of their latest vendor-designed

fuels.

The inspectors

also noted that upon receipt of the vendor 's November

notification the licensee's

follow-up response to the notification was

prompt, reasonable

and was considered

adequate.

The licensee's

response

was also adequate

considering that Unit 3 was in coastdown condition

(for a February outage)

and the unit was not in a full-rated power

conditions.

0

0

0

E6.1

a.

12

Engineering Organization

and Administration

En ineerin

Staff Over time

Ins ection Sco

e

37551

As a part of routine core inspection activities, the inspectors

reviewed

hourly regular

time and overtime records for licensee

system/technical

engineering

and radiation control

(RADCON) group personnel.

b.

Observations

and Findin s

During the inspection period the inspectors

reviewed

a selected

week of

data during the month of September

1996 hourly regular time/overtime

work records for licensee

system/technical

engineering

and

RADCON

personnel.

The inspectors

noted that

BFN system engineering

group

personnel,

on average,

worked approximately 47 hour5.439815e-4 days <br />0.0131 hours <br />7.771164e-5 weeks <br />1.78835e-5 months <br /> s per. week.

This

average

was slightly higher

than that experienced

by most of the

engineers

in the group (approximately 42 hours4.861111e-4 days <br />0.0117 hours <br />6.944444e-5 weeks <br />1.5981e-5 months <br /> per week)

due to one

individual working about

66 hours7.638889e-4 days <br />0.0183 hours <br />1.09127e-4 weeks <br />2.5113e-5 months <br /> in one week whjle another worked about

62 hours7.175926e-4 days <br />0.0172 hours <br />1.025132e-4 weeks <br />2.3591e-5 months <br />.

Two other

system engineers

worked about

53 hours6.134259e-4 days <br />0.0147 hours <br />8.763227e-5 weeks <br />2.01665e-5 months <br /> during the

selected

week in September.

The inspectors

also noted that technical

engineering

department

personnel

worked approximately 41 hours4.74537e-4 days <br />0.0114 hours <br />6.779101e-5 weeks <br />1.56005e-5 months <br /> per week.

A minimal amount of overtime was used by the technical

engineering

group

personnel.

The inspectors

noted that

RADCON personnel

used very little

overtime and on average

worked

=a straight 40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br />

per

week.

C.

Conclusions

The inspectors

.found that licensee

personnel

in the above work groups

used very little overtime.

The "40-hour work week" appeared to be the

norm for most personne1

in the identified -groups.

None of the reviewed

records presented

any indications nor evidence that licensee-approved

overtime limitations, .as presented

in SSP-1.7,

Overtime Restrictions-

Regulatory,

(this SSP implements elements of NRC Gener ic Letters 82-12

and 83-14),

had been exceeded.

The inspectors

found that licensee

'ystem engineering,

technical

engineering

and

RADCON personnel

weekly

working hour averages

were not out of the ordinary and over time to be

adequately controlled.

E8 Miscellaneous

Engineering

Issues

E8.1

Fuse

Pro

ram Activities

a.

Ins ection Sco

e

37551

The inspectors

reviewed activities associated

with the licensee's

fuse

program.

The inspectors

also performed

a follow-up inspection of

identified-fuse modification drawing discrepancies,

fuse identification

issues,

and past problems of incorrectly identified fuse installations.

0

~ ~

~

b.

Observations

and Findin s

13

During the inspection period, inspectors

followed-up on 28

PERs which

dealt with various fuse program activities in order to determine the

significance of the licensee identified problems.

All 28

PERs

had been

written since January

1996.

During 1996 the following fuse-related

PERs appeared:

~

Nine blown fuses.

Two of these

were related to problems with the

Unit 2 Shutdown Board

(SBD)

Room chiller fuses.

The remaining

seven failures were unrelated,

isolated events.

~

Five noted drawing discrepancies;

i.e., the drawi,ngs did not

reflect current/actual

plant configurations.

Equipment

was not

safety-related

and drawings are being revised using normal

licensee-approved

drawing discrepancy corrective action practices.

~

Three involved improperly installed fuses

and six described

incorrectly identified fuses.

Field identification of fuses is

part of a new initiative which is currently being implemented.

The improperly installed fuses involved non-safety equipment.

~

Five described

miscellaneous

fuse issues; i.e., insufficient

stock,

inadequate

stock, inappropriate

design or inaccurate

fuse

labeling issues.

An updating of current fuse stock and purchase

of safety fuses is on-going.

Dedication of non-safety fuses for

use in safety-related

systems is also on-going and appears to be

adequate.

c.

Conclusions

The inspectors

determined that the high number

of. fuse related

PERs are

due to a combination of a new initiative for field identification,

and

a

low threshold for identifying issues

including non safety-related

equipment.

The licensee's

current

PER process appropriately

and

correctly addresses

on-going fuse issues.

E8.2

0 en

VIO 50-260 296/EA 95-220:

This violation identified that on

Fe ruary 2 and 4,

1993, the licensee failed to ensure that provisions

of 10 CFR 50.7 were implemented,

in that, .Stone

and Webster Engineering

- Corporation

(SWEC),

a contractor to the Tennessee

Valley Authority (TVA)

at the Browns Ferry .Nuclear Plant discriminated against

a worker engaged

in protected activities.

A Region II inspector held discussions

and

performed inspections with TVA and. SWEC personnel

to assure

corrective

actions for this violation had been properly implemented.

The inspector

reviewed the following corrective action documents:

~

SWEC Hanagement

memorandum dated September

14,

1993, advising

supervisors

and managers of their responsibility in the area of

employee protection.

Ch

0

14

~

'Documentation of tool box meetings

held September

20,

1993, that

discussed

the employees rights to discuss

and report employee

concerns to SWEC,

TVA or the

NRC.

~

HEADS-UP Bulletin issued

September

20,

1993, to all

SWEC

personnel.

This Bulletin discussed

SWEC's open door policy and

available

avenue

for employees to express

any safety concerns

without-fear of reprisal.'

Survey results

conducted

by SWEC on October

6-11,

1993,

and

Harch 28,

1994.

In addition to the above listed corrective actions,

the inspector

reviewed documentation

recently issued

by TVA that emphasized

TVA's

continuing support of eliminating harassment

in the workplace.

This

documentation

included

a combined

memorandum

from the Browns Ferry Site

Vice President

and Plant Hanager dated July 29,

1996,

and another

memorandum

from the TVA President,

dated August 7, 1996, that reiterates

that employee intimidation. harassment,

discrimination, or retaliation

for expressing

concerns will not be tolerated.

This violation will remain open pending the outcome of the

SWEC appeal

to the United States

Court of Appeals for the Eleventh Circuit as

discussed

in NRC's letter dated February 14,

1996,

on this subject.

The

inspector's

review determined the licensee's

contractor,

SWEC had

complied with the corrective actions specified in the response to the

violation.

Additionally, the inspector

found the licensee

had also

taken corrective actions relative to notifying TVA employees

and

contr actor personnel

that intimidation and harassment

at the TVA nuclear

facilities will not be tolerated.

IV. Plant Su

rt

Radiological Protection

and Chemistry Controls

Uncontrolled Locked Hi h Radiation Area

Ins ection Sco

e (71707,

71750)

On .December

27,

1996, the licensee identified an Uncontrolled Locked

High Radiation Area.

The inspectors

reviewed the licensee's

Incident

Investigation

Repor t (IIR); Operating Instruction 3-0I-6, Feedwater

Heating and Hisc Drains System,

Revision 9;

and Site Standard Practice

SSP-12.1,

Conduct of Operations,

Revision 30.

Observations

and Findin s

On December

27,

1996, the licensee's

RADCON group identified that

an

uncontrolled Locked High Radiation Area

(LHRA) existed in the Unit 3

3Al/3A2 Heater

Room.

During normal plant operations,

the room is posted

as

a LHRA, but had been de-posted to support maintenance activities when

0

0

15

extraction

steam

had been isolated.

The area

became

a

LHRA again

when

operations

personnel

inadvertently introduced

a radiation source to the

room by manipulating

an extraction

steam valve.

The IIR stated that the

area

remained

as

an uncontrolled

LHRA f'r approximately four hours.

The area

was still posted

as

a contamination

zone

and as such access

was

controlled by a Radiation Work Permit

(RWP).

Although unanticipated

radiation exposures

had occurred,

the maximum individual dose received

by any of the

5 individuals who entered the area during the time frame,

while the uncontrolled

LHRA existed,

was 31 mrem.

The doses

received

did not exceed the alarm setting of 140 mrem integrated

dose

on licensee

electronic dosimeters

worn by the workers,

nor did unexpected

doses

received

by the workers exceed

10 CFR 20.1201 limits.

The. licensee's

IIR indicated that the area

was immediately re-posted

as

a

LHRA by a

RADCON technician

upon discovery,

and the area

was manned

until both accesses

were locked.

The licensee's

IIR identified the following three findings:

~

(Finding gl) Sufficient administrative controls were not in place

to ensure that the

HP heater

room was controlled as

a

LHRA prior

to changing plant conditions.

Proper controls were not in p'lace to

ensure applicable criteria were met.

The procedures

for putting

heaters

in service did not contain adequate

guidance to notify

RADCON when extraction

steam

was to be returned to service.

~

(Finding $2) Inappropriate/incomplete

communications contributed

to the event.

The, Unit Super visor (US) and AUOs did not accurately

communicate

requirements of RADCON involvement.

In addition, pre-

job and

RADCON briefs were incomplete

and inaccurate.

The pre-job

brief did not include

RADCON considerations

and failed to discuss

all planned activities and radiological conditions.

Furthermore,.

the

RADCON brief -for the AUOs/EHs was misleading

and inaccurate,

in that, it stated

expected

doses

should be I to 2 mrem/hr.

~

(Finding g3) Plant personnel

involved in this event were not fully

aware of actual- radiological conditions

nor all work activities in

the 3A1/3A2 feedwater,heater

rooms.

The IIR further states that

personnel

did not exhibit the necessary

"questioning attitude"

and

use of BFN's STA'R concept during this event.

c.

Conclusions

The inspectors

determined that,

as described in licensee finding number

one, Operating Instruction 3-0I-6, Feedwater

Heating

8 Misc Drains

System,

Revision 7, was not adequate to ensure

RADCON was notified of

the changing plant conditions which caused

a rise in area radiation

levels.

This is identified as the first example of an inadequate

procedure violation (50-296/96-13-03).

lh

0

0

16

In addition, the inspectors identified that SSP-12.1,

Conduct of

Operations,

Revision 30,

was inadequate to ensure that radiological

control personnel

were appropriately informed prior to evolutions

or

activities that have

a potential to significantly change radiological

conditions in the plant.

Procedure

SSP-12.1,

Section 3.4.5.G,

Radiological Protection,

states

radio1ogical control personnel

should be

informed prior to evolutions

or activities that have

a potential to

significantly change radiological conditions in the plant.

As worded,

the procedure

was not adequate

to require proper notification to

radiological personnel,

because

the word "should" is defined

as

a

recommendation

in SSP 2.2, Writing Procedures.

Admission of extraction

steam to the feedwater heaters

in an uncontrolled area of the plant was

considered

by the inspectors to be an evolution that significantly

changed radiological conditions in the area.

This issue is identified

as

an second

example of an inadequate

procedure violation

(50-296/96-13-03).

The licensee's

IIR did not address

the inadequate

Conduct of Operations

procedure

described in the second

example of the violation.

In

addition, the licensee's

corrective actions failed to specifically

address

licensee expectations

for pre-job briefings and

how those

expectations

would be conveyed to the licensee's staff.

V. Mana ement Meetin s

Xl

Exit Meeting Sumary

An exit meeting concerning Engineering

and

SWEC (Section E8.2)

was

conducted

on December

20,

1996.

The Region II-based inspector described

areas

inspected

and discussed

in detail inspection results.

A listing

of inspection findings is provided.

Proprietary information is not

contained in this report.

Dissenting

comments

were not received

from

the licensee.

The resident

inspector s pr esented

overall inspection period results to

licensee

management

on January

10,

1996.

The licensee

acknowledged the

findings .presented.

'Proprietary information involving reactor fuel was

reviewed,

and proprietary information. was not included in this

inspection report.

Licensee

PARTIAL LIST OF PERSONS

CONTACTED

T. Abney, Licensing Hanager

J. Brazell, Site Security Manager

G. Bugg, Acting Manager,

Radiological Control

and Chemistry

R. Coleman, Acting Radiological Control

Manager

C. Crane, Acting Plant Hanager

J

~ Grafton, Chemistry Representative

Ik'

II

0

0

'

17

,M. Harding, Concerns Resolution

Program

Manager

(Chattanooga)

J. Johnson,

Site Quality Assur ance

Manager

R. Jones,

Operations

Manager

S.

Kane, Licensing Supervisor

R. Kent-Ryan,

Employee Concerns

Representative

(SWEC)

'G. Little, Operations

Superintendent

R. Hachon, Site Vice President,

Browns Ferry

D..Hatherly, Licensing

Representative'.

Pierce,

System Engineering

Manager

E. Preston,

Plant Manager

T. Shriver,

Nuclear Assurance

and Licensing Manager

K. Singer,

Maintenance

Manager

J.

Thompson,

Employee Concerns Representative

(TVA Browns Ferry)

R. White, Operations Supervisor (Fire Protection)

H. Williams, Engineering

and Materials Manager

IP 37551:

IP. 62707:

IP 71707'P

71750:

IP 92050:

IP 92700:

IP 92901:

IP '92902:

IP 93702:

INSPECTION PROCEDURES

USED

Onsite Engineering

Maintenance

Observations

Plant Operations

Plant Support Activities

Review of Quality Assurance for Extended Construction Delays

Onsite Followup of Written Reports of Nonroutine Events at Power

Reactor Facilities

Followup-Plant Operations.

Followup-Maintenance

Prompt Onsite Response to Events at Operating

Power Reactors

~Oened

ITEMS OPENED

CLOSED

AND DISCUSSED

'VIO

'URI

VIO

Item Number

Status

50-260/96-13-01

Open

50-259,260,296/

Open

.96-13-02

50-296/96-13-03

Open

Descri tion and Reference

Failure to Implement Licensee-

Approved Work Controls for Changes

to the

SFP (Section H2.1)

Tool Pouch Issues

(Section M1.2)

Uncontrolled Locked High Radiation

Area (Section R1.1)

0'

'

. "Closed.

T~,

LER

Discussed

IFI

Item Number

Status

50-296/95-004-00

Closed

Item Number

Status

50-296/96-08-02

Open

18

Descri tion and.Reference

Unplanned

ESF Actuation Fol:lowing

Transfer of 480V Shutdown Board 3A

To Its Alternate Supply

(Section 08.1)

Descri tion and Reference

Emergency

Core Cooling System

Inverter Failure (Section 02.2)

VIO

50-260,296/

EA95-220

Open

Browns Ferry Discrimination.

Against Worker Engaged In

Protected

Activities (Section E8.2)

~l

~

'

0