ML18038B542

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Insp Repts 50-259/95-56,50-260/95-56 & 50-296/95-56 on 950917-1014.Violations Noted.Major Areas Inspected: Operations,Maint & Surveillance Testing Activities,Unit 3 Restart Including Numerous Equipment Testing Activities
ML18038B542
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 11/07/1995
From: Lesser M, Wert L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18038B540 List:
References
50-259-95-56, 50-260-95-56, 50-296-95-56, NUDOCS 9511160055
Download: ML18038B542 (78)


See also: IR 05000259/1995056

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W., SUITE 2900

ATLANTA,GEORGIA 303234199

Report Nos.:

50-259/95-56,

50-260/95-56,

and 50-296/95-56

Licensee:

Tennessee

Valley Authority

6N 38A Lookout Place

1101 Market Street

Chattanooga,

TN

37402-2801

Docket

Nosg I

50-259,

50-260,

and 50-296

License

Nosg I

DPR-33,

DPR-52,

and

DPR-68

Facility Name:

Browns Ferry Units 1, 2,

and

3

Inspection at Browns Ferry Site near Decatur,

Alabama

Inspection

Conducted:

September

17 - October

14,

1995

Inspector:

~O

Leonar

.

er

,

r., Senior

Ress

ent

nspector

J.

Hunday,

Resident

Inspector

R. Musser,

Resident

Inspector

H. Morgan, Resident

Inspector

ate

sgne

Approved'y:

Har

.. esser,

C

>e

,

Reactor Projects

Branch

6

Di'vision. of Reactor Projects

SUMMARY

Scope:

This routine resident

inspection

involved inspection on-site'n

the areas of

operations,

maintenance

and surveillance testing activities, Unit 3 restart

activities including numerous

equipment testing activities,

and review of open

items,

including several

Three Mile Island Action Items.

Several

hours of

backshift coverage

were routinely worked during most work weeks.

Deep

backshift inspec'tions

were conducted

on September

26,

30, October

1, 7, 8, 9,

10,

13,

and

14.

Enclosure

2

95iii60055 95ii07

PDR

ADOCK 0500025'7

Q

PDR

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Results:

One violation and

one inspector followup item were identified:

Operations:

One violation was identified involving improper actions

by a control

room

senior reactor operator during

a Unit 3 testing activity.

Failure to follow

the actions of the alarm response

procedure

resulted

in de-energization

of a

480 volt, shutdown

board

and inadvertent

engineered

safety feature actuations.

(VIO 296/95-56-01:

Failure to Follow Alarm Response

Procedures

Results

in Loss

of 480V. Bus,

paragraph

2.3)

A NRC inspector identified that watchstander

actions involving the traveling

water screens

had not been properly communicated

to the Unit 2 control

room.

High differential pressure

across

the screen

was not being effectively

monitored.

Additionally, maintenance

personnel

were not actively cleaning

the trash racks

as expected.

The incident indicated that

some personnel

are

not yet sensitive to aspects

of multiple unit operations.

(paragraph

2.2).

Maintenance

and Surveillance:

An inspector followup item was identified associated

with the

use of a nickel

based

thread lubricant

on gaskets

in fluid systems.

(IFI 50-260/95-56-02,

Use

of Nickel-Based

Thread Lubricants

on Gaskets

in TVA Class

"B" Fluid Systems,

paragraph

3.2)

During observation of Unit 2 surveillance tests,

the inspectors

identified two

issues

in which enhancements

to the procedural

guidance

would improve the

quality of the testing.

(paragraph

3. 1)

Unit Three Recovery:

Extensive monitoring of Uni,t 3 recovery activities

was conducted'.

Numerous

major tests

were observed

and reviewed:

The i'nspectors verified that drywell closeout

and unit separation activities

were prog'ressing

well and were adequate

to support the restart.

(paragraphs

4.2

and 4'.5)

Reviews of the Unit 3 Environmental gualification activities indicated that

the program is being adequately

implemented.

(paragraph

4.7)

The inspectors

reviewed the status of Corrective Action Tracking Documents

and

concluded that the licensee's

program to track and resolve the items

has

been

effective.

(paragraph

4.9)

During review of Nuclear Performance

Plan issues,

the inspectors

identified

some deficiencies

on

a flow drawing of the high pressure

coolant injection

system control oil piping.

Subsequent

review confirmed that the associated

modification work to the governor system

had

been

completed properly

and the

items were drawing inaccuracies.

(paragraph

4. 10)

I

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Testing of the residual

heat

removal

system,

high pressure

coolant injection

system,

control air systems,

main steam isolation valves,

and reactor core

isolation cooling system

was monitored

by the inspectors

(paragraph

4.8).

Other, equipment testing,

including the control

rod drive system,

was observed

or reviewed

.in detai',1- to support closure of open

items

(paragraph

5.0).

Several

deficiencies

associated

with valve position status

(paragraphs

4.8.2

and 4.8.4)

were identified.

While the involved systems

were not yet required

to be operable

at the time, the inspectors

noted that the licensee's initial

actions

in response

to the:specific

problems

were not aggressive.

One example

of improper operator actions

(paragraph

2.3)

was noted.

Overal=l, the testing

was conducted

properly

and emergent

issues

were identified for resolution

as

required.

I

'4

if'

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REPORT DETAILS

1.0

Persons

Contacted

Licensee

Employees:

T. Abney, Unit 3 Nuclear Assurance

and Licensing Manager

J. Brazell, Site Security Manager

R. Coleman,

Radiological Controls Manager

  • J. Corey,

Chemistry

and Radiological Controls Manager

T. Cornelius,

Emergency

Preparedness

Manager

~C. Crane,

Assistant

Plant Manager

  • J. Johnson,

Site guality Manager

R. Jones,

Unit 3 Startup

Manager

  • G. Little, Operations

Superintendent

R. Machon, Site Vice President,

Browns Ferry

J.

Haddox,

Maintenance

and Modification, Manager

  • R. Moll, Plant Operations

Manager

  • G. Pierce,

Technical

Support

Manager

E. Preston,

Plant Manager

S.

Rudge,

Site Support

Manager

J.

Sabados,

Chemistry Manager

  • P. Salas,

Licensing Manager

T. Shriver,

Nuclear Assurance

and Licensing Manager

D. Stinson,

Recovery

Manager

  • S. Wetzel, Acting Compliance

Licensing Manager

  • J. White, Outage

Manager

H. Williams, Engineering

and Materials

Manager

Other licensee

employees

or contractors

contacted

included licensed

reactor

operators,

auxiliary operators,

craftsmen,

technicians,

public safety

officers,

and quality assurance,

design,

and engineering

personnel.

NRC Personnel:

  • L. Wert, Senior Resident

Inspector

  • J. Hunday,

Resident

Inspector

  • R. Husser,

Resident

Inspector

M. Morgan, Resident

Inspector

G. HacDonald,

DRS Inspector

C. Patterson,

Senior Resident

Inspector,

Brunswick

J. Williams,

NRR Project Manager

G.

Wiseman,

DRS Inspector

  • Attended exit interview

Acronyms

and initialisms used throughout this report are listed in the last

paragraph.

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2.0

Plant Operations

(71707,

92901,

71750,

40500)

2. 1

Operations

Status

and Observations

Unit 2 operated

at power during this inspection period.

Activities within the

control

rooms were monitored routinely.

Inspections

were conducted

on day and

night shifts, during weekdays

and

on weekends.

Observations

included control

room manning,

access

control, operator professionalism

and attentiveness,

and

adherence

to procedures.

The inspectors

noted that operators

were cognizant

of plant conditions

and were attentive in their duties.

Due the approaching

Unit 3 restart,

the inspectors

have emphasized

review of issues that have

potential affects

on the operation of the other unit.

Paragraph

2.2 describes

a problem involving poor communications

between

some operations

personnel.

Instrument readings,

recorder traces,

annunciator

alarms, operability of

nuclear instrumentation

and reactor protection

system channels,

availability

of power sources,

and operability of the Safety Parameter

Display System were

monitored.

Control

room observations

also included

emergency

core cooling

system lineups,

primary and secondary

containment integrity, reactor

mode

switch position,

scram discharge

volume valve positions,

and rod movement

controls.

The inspectors

noted that

on

some occasions,

the pace of Unit 3

testing activities in preparation for fuel loading stressed

the Unit 3 control

room personnel.

The large

number of ongoing activities

may have contributed

to some noted lapses

in CR performance

during the period.

(paragraphs

2.2,

2.3,

and 4.8.)

Daily discussions

were held with plant management

and various

members of the

plant operating staff.

One of the inspectors

attended'the

daily Plan of the

Day meetings.

Plant tours were taken throughout the reporting period

on

a

routine basis.

Observations

included valve position

and system alignment,

snubber

and hanger conditions,-containment

isolation alignments,

instrument

readings,

housekeeping,

power supply and breaker alignments,

radiation

and

contaminated

area controls,

tag controls

on equipment,

work activities in

progress,

and radiological protection controls.

Informal discussions

were

held with plant personnel

during these tours.

The tours in the Unit

1 areas

focused

on maintenance

activities

and

systems

required to be operable

to ensure that appropriate attention is provided to

the shutdown unit.

The inspectors

toured the protected

area

and noted that the perimeter

fence

was intact

and not compromised

by erosion or disrepair.

The fence fabric was

verified to be intact

and secured.

The inspectors

also observed

personnel

and

packages

entering the protected

area

and verified they were searched

either

by

special

purpose detectors

or physical

patdown.

2.2

Traveling Water Screen

High Differential Pressure

On September

20,

1995, while .touring the Unit 2 main control

room, the

inspector

noted that the annunciator for circulating water traveling screen

high differential pressure

was in alarm.

The differential pressure

at that

time was approximately

10 inches of water.

Additionally,. it was noted that

the traveling screens

were not in service.

The inspector

informed the unit

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ASOS who was

unaware of the condition.

He indicated that Unit 3 Operations

personnel

were controlling activities associated

with keeping the trash

racks

and screens

clear of debris.

After contacting the Unit 3 ASOS, Operations

personnel

were dispatched

to place the traveling screens

in service

and

maintenance.

was contacted

to scrape

the trash racks.

Further discussion

indicated, that the

AUO responsible

.for operations

at the intake structure

had

contacted

the Unit 3 control

room earlier

and informed them that

he was

securing

the traveling screens

and leaving the area,

however the Unit 2

control

room was not contacted.

At the time of the event Unit 2 was at

100

percent

power

and

was the unit most affected

by this condition.

With the

alarm sealed

in as it was,

the control

room staff would have received

no

warning that the condition was worsening.

Additionally, site

management

had

determined

the previous

week that the trash racks

needed

to 'be cleaned

around

the clock because

of the sudden

insurge of aquatic grass.

At that time the

differential pressure

was less

than

8 inches of water.

At the daily plan of

the day meeting

on September

20, the inspectors

had noted discussion

indicating that maintenance

personnel

were cleaning the racks continuously.

The inspectors

noted that

no maintenance

personnel

were present

at the intake

to clean the racks

when the issue

was identified.

Apparently there

were

some

coordination

problems involving maintenance

personnel.

Subsequently,

the

inspectors

observed

trash rack cleaning activities

and cleaning of material

from intake water with a specially equipped

boat.

The inspectors

concluded that this event

was the result of miscommunication.

The incident indicated that

some Operations

personnel

are not yet

appropriately sensitive to aspects

of multiple unit operations.

Discussions

were held with site management

concerning this conclusion.

Subsequently,

the

licensee initiated

BFPER951321

to document the problem

and develop corrective

actions

which included discussion

with essentially all onsite

personnel

of the

issue

as

a "dual unit incident".

2.3

Inadvertent

ESF Actuations

Caused

By Improper Operator Actions

On October 7,

1995

a .loss of the

3A 480V Shutdown

board occurred

due to

improper actions

by an

SRO in the Unit 3 control

room.

The loss of the

bus

resulted

in

a de-energization

of the "B" reactor protection

system

bus

and

several

inadvertent

ESF, actuations.

Testing, to investigate

a problem noted during previously completed

"B" EDG

load acceptance

testing

was in progress.

With the

"B" EDG supplying

power to

the

"3EB" 4

kV shutdown board,

the

EDG unexpectedly

tripped

due to

a loss of

field as loads

were applied.

When the

"B" EDG output breaker

opened,

this caused

a loss of power to the

3EB

shutdown

board

and consequently

transformer

TS3E which is the backup supply to

the

3A 480

V shutdown

board.

The loss of the transformer

power caused

annunciator

"480V SD

BD 3A UV or XFER" to be illuminated on

a control

room

panel.

The

3A 480

V .SD board continued to be powered

from TS3A and

4KV board

3EA.

A SRO in the control

room incorrectly transferred

the board to the its

"alternate

source"

which Was the de-energized

feeder

from TS3E.

This caused

a

loss of one

RPS

bus

and the

ESFs.

All ESF equipment

performed

as expected.

15

if'gal

One of the inspectors

reviewed the available documentation

of the event,

discussed

the incident with the involved personnel,

and conducted

additional

review.

A pre-job briefing had

been

completed

and the testing

sequence

was

set forth in the text of an approved

Work Order.

The involved

SRO

acknowledged

that=he

had

made

an error in transferring the board.

The

inspector

reviewed Alarm Response

Procedure

3-XA-55-8B.

The procedure listed

loss of supply breaker

as

a cause

and requires, operator to "check for

indication of 480V shutdown

board

3A loss".

The procedure

also states; "If

the board is lost, then manually transfer the board".

While the wording on

the annunciator

window seems

to be misleading,

.the inspector verified through

discussion

with operators

that control

room personnel

are trained

and

aware

that the alarm can

be caused

by

a loss

of. the alternate

supply breaker.

The

inspector also noted that the readily available

480V board voltage indications

are located

on the

EDG panels

about

10 feet

away from the alarm

and transfer

switch locations.

(The voltage

can

be obtained at the switch panel

by

selection of the individual board

and reading

a voltage indication with input

from several different boards.)

The inspector

noted that the control

room log entries

associated

with the

i'ncident were very brief and did not contain sufficient details for a reviewer

to understand

some of the factors in the event.

The maj'or concerns

in the incident involved the improper actions

by the senior

reactor operator.

While it is recognized that

some personnel

errors

may occur

during the performance of evolutions,

in this instance

several

significant

deficiencies

were noted.

Pl,ant

management

has

been

emphasizing

the

need to

improve per'formance

so that these

type of incidents

are prevented.

As an

SRO,

this individu'al has

a responsibility to maintain control

and oversight over

the control

room activities.

The

SRO does

not normally operate

control

room

switches.

He became

involved in the details of the incident

and apparently

focused

in on one lit annunciator.

The

SRO did not comply with the actions in

the alarm response

procedure.

The

SRO did not utilize the self verification

techniques

currently being

emphasized

by licensee

management.

As the

SRO,

he

is not only expected

to use the techniques

but he is relied

upon to ensure

that the other control

room operators

apply the techniques.

The present

conditions of Unit 3 did not require

such rapid actions

on

a loss of the 480V

bus.

Operations

management

initiated corrective actions including counseling of the

involved

SRO; discussion of the incident during shift turnovers,

and

preparation of an "immediate reading"

package

on the incident.

" Immediate

readings"

are required to be read

by all Operations onshift personnel

prior to

assuming duties.

The inspector verified .that the reading

packages

were being

reviewed

and signed.

The failure of the

SRO to follow the alarm response

procedure

is

a violation.

This issue is identified as

VIO 296/95-56-01:

Failure to Follow Alarm Response

Procedures

Results

in Loss of 480V Bus.

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2.4

Failure of Secondary

Containment Isolations

Dampers

To Isolate

On October 4,

1995,

whil'e swapping the inservice reactor

zone ventilation

fans,

the inboard

and outboard

supply isolation dampers,

2-FCO-64-13

and

14,

failed to isolate

as required.

The licensee

entered

TS 3.7.C.2 which required

secondary

containment integrity to be restored within four hours or place the

reactor in Hot Shutdown within the following twel.ve hours.

Operators

were

dispatched

to investigate

and determined

the problem to be due to sticking

solenoid valves.

The solenoids

were lightly tapped

and the dampers

closed

as

required.

The dampers

.were subsequently

cycled three additional

times to

provide assurance

that this was the cause of the failure.

The remaining

secondary

containment isolation dampers

were also cycled to verify they

operated

properly.

On October

5, the

1-FCO-64-14 failed to isolate

and the

cause.

was again determined to be due to

a sticking solenoid valve.

In this

case

the other damper in series

was isolated

and the system

secured,

Technical Operability Evaluation 2-95-064-1413

was written to determine

the

operability status of the dampers.

The

TOE stated that the affected valves

were operable

but that they needed

to be stroked daily until the solenoids

were replaced.

This was performed

on October

10 and

11.

The

TOE directed

that

upon experiencing

a subsequent

failure of a damper to close

due to

a

sticking solenoid,

the damper could be

made operable

by successfully

stroking

it three successive

times

and then

once per day until the solenoid is

replaced.

If the damper failed again before the solenoid could

be replaced

an operator'ould

be continuously stationed

at the damper to ensure

that it

closes

upon actuation of an isolation signal.

Paragraph

3. 1. 1 of this report

describes

additional

NRC review of this issue.

The inspectors will continue

to monitor the licensee's

actions to resolve the solenoid valve issues

and

concluded that the licensee's

actions to date

have

been

adequate.

One violation was identified.

3.0

Maintenance Activities and Surveillance Testing

(62703,

92902,

61726,

92901,

37551,

92903)

3.1. 1 Maintenance

Observations

Maintenance activities were observed

and/or reviewed during the reporting

period to verify that work was performed

by qualified personnel

and that

approved

procedures

in use adequately

described

work that was not within the

skill of the trade.

Activities, procedures,

and work requests

were examined

to verify proper authorization to begin work, provisions for fire hazards,

cleanliness,

exposure control, proper return of equipment to service,

and that

limiting conditions for operation

were met.

The following maintenance activities were reviewed

and witnessed

in whole or

in part

WP 19785-79.80

4kV Shutdown

Board

3EA Modification (Rework of Internals

and

Termination of Cabling/Wiring)

if'gl

On September

19,

1995,

an inspector

observed

the terminator ("re-termination"

of cabling/wiring) portion of the

3EA Shutdown

Board modification.

Specific

leads

associated

with the

3A Core Spray

Pump motor were landed

and the

inspector

noted that the "cutback" of wiring insulation appeared

satisfactory

with no observance

of stray wiring cuts.

The wiring lugs also

appeared

satisfactory

and were of the type required

by the procedure.

Crimping of the

wire lugs to the wires was performed correctly.

The breaker

was

satisfactorily tested after the re-termination activities were performed.

Specifics of the work package

and operation of the

3A Core Spray

pump were

appropriately performed.

WO 95-18326-00

Secondary

Containment

Inboard Isolation

Damper Solenoid

Valve Replacement

'I

On October

10,

1995,

the inspector witnessed

the replacement of the solenoid

valve for the secondary

containment

inboard isolation damper,

2-FC0-64-14.

The solenoid

was being, replaced

because it had failed to properly operate

during previous cycles

as described

in paragraph

2.4.

The inspector

attended

the prejob brief which was attended

by the maintenance,

engineering,

and

operations

personnel

involved in the activity.

The participants

were not well

prepared, for the activity as evidenced

by the following examples; it was not

clear if the work would be performed with the solenoid energized

or

deenergized,

there

was confusion over whether old or new air line fittings

would be used

and

when it was decided to use

new fittings they were not

available,

and questions

concerning

what the proper post maintenance

test

should

be.

Although it was expected that these details

should

have

been

worked out prior to the briefing they were resolved prior to commencing work.

The actual

work in the field was completed with no problems

noted.

The damper

was stroked following completion of the work and performed satisfactorily.

The solenoid which was

removed

was given to engineering for causal

analysis of

the failure.

3. 1.2 Surveillance

Observations

Surveillance tests

were reviewed

by the inspectors

to verify procedural

and

performance

adequacy.

Testing

was witnessed

to ensure that approved

procedures

were used, test equipment

was calibrated,

prerequisites

were met,

test results

were acceptable,

and system restoration

was completed.

2-SI-4.5.C. I(3)

-RHRSW

Pump

And Header Operability

And Flow Test

This test is performed to verify operability of the

RHRSW pumps in accordance

with TS and to meet the requirements

of the

ASME Section

XI program.

Portions

of this surveillance

were observed

by the inspector

on September

25,

1995.

While testing the

02

pump the inspector

noted that the vibration data

was

taken while the

pump was operating at maximum flow.

After vibration data

was

taken the

pump .flow was decreased

to obtain

a specified discharge

head.

This

flow rate

was recorded

on the section

XI data sheet.

The inspector questioned

the operator

about

why the specified discharge

head

was not first established

prior to taking the vibration data.

The operator conducting the test stated

that Section

7. 14 of the procedure

required that the data

be taken with the

pump at full flow.

The inspector questioned this because

the

pump

maximum

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flow rate will decrease

as the

pump degrades.

If the. vibration data is not

taken

each

time with the

same

pump conditions,

the information would not be

useful for trending.

The operator

agreed

and requested

engineering

support.

The system engineer

stated that the vibration data

should not be taken at full

flow but rather at the flow required to obtain the specified discharge

head.

Based

on this information, Operations,

determined that the information

obtained

was invalid and reperformed

those portions of the specific test.

Technical

Support revised the surveillance

procedure

to clarify these

sections

of the procedure.

The inspector

asked the licensee to determine if the

operability of any of the

pumps would be challenged if the previous

performances

of this surveillance

were also performed

wrong with the

pump at

full flow.

Technical

Support

compared

the vibration data with the

pump at

full flow with the vibration data with the

pump at the required test flow.

This review indicated that the point of highest vibration with the

pump at the

flow required

by the test

was approximately

one

and one-half times the

vibration with the

pump at full flow.

Technical

Support then multiplied the

vibration readings for the remaining

pumps

by four to see if this value would

be high enough to result in any of the

pumps

becoming inoperable.

This review

indicated that if the surveillance

was performed this way in the past

and the

data collected

was actually done

so with the

pump at full flow, the vibration

readings

would still be below that requiring action.

The inspectors

concluded

that the safety significance if-the specific testing

issue

was not large

and

the corrective actions

were sufficient.

During the surveillance

the inspector also noted that the

RHR System

I flow

recorder

2-FR-74-64 spiked

when

any of the

Loop I

RHRSW pumps were started or

stopped.

Simple troubleshooting

could not identify the cause.

Work order 95-

17904-00

was written to troubleshoot

the circuit further and facilitate

repairs.

2-SI-4.3.C

Scram Insertion

Times

On September

30,

1995,

the inspector witnessed

portions of the performance of

this procedure.

This surveillance

manually scrams

individual control

rods

and

measures

the amount of time necessary

for the rod to travel full in.

An

evaluation of control rod performance

is then

made.

The inspector witnessed

portions of this surveillance

both in the control

room and locally at the

individual hydraulic control units.

While in the control

room, it was noted

that the blue lights indicating that the control rod scram valves

were

open

did not always illuminate when the scram valves were open.

After manually

exercising the limit switches

the blue lights illuminated.

This occurred for

approximately half of the nineteen

rods tested.

The valve limit switches

provide

no function except to illuminate the blue lights in the control

room

and therefore

work orders

were generated

to perform repairs at

a later date.

To perform this surveillance,

the charging water for the control rod being

tested

was isolated to ensure that the rod is being

scrammed

from accumulator

and reactor pressure

only.

While observing the activities of the operator at

the hydraulic control unit the inspector noted that charging water isolation

valve manipulations

were not being independently verified.

The operator

was

questioned

and stated that it was not

a requirement of the procedure.

The

inspector

reviewed the surveillance

procedure

as well as the normal operating

procedure

and confirmed that the procedure

did not require

independent

Igi

gl

i/i

verification.

However, at the conclusion of the surveillance,

BFPER951392

was

written stating that the procedure

did not require independent verification at

the completion of the testing.

Operations

then independently verified the

correct position of all the valves manipulated

during the performance of the

surveillance.

None were found out of position.

At the close of this report

period, Operations

management

had not yet decided if the valves

were going to

be included in the list of equipment requiring independent verification.

This

will be resolved

as part of the closeout of the

PER.

Section 4.8 of the report describes

NRC review of Unit 3 testing

and

maintenance activities.

The above surveillance

observations

indicate that

specific testing

procedures

could

be improved.

3.2

Use of Nickel-Based

Thread Lubricants

on Gaskets

in Class

"B" Fluid

Systems

On August 24,

1995, during

a routine observation of condensate

system

check

valve maintenance,

a licensee

QA inspector, noted that the "pipe flange to

valve joint" gaskets

.were coated with a nickel-based

thread lubricant ("Never

Seez").

The

QA inspector

noted that

such action potentially allowed this

nickel-'based

thread lubricant to be in direct contact with the condensate

system water.

Leeching of this lubricant into the condensate

system

was highly

probable.

The inspector

noted that,the

WO did not specifically .identify'ny

gasket lubrication for this job and the j'ob foreman stated that lubrication of

the gaskets

with this nickel-based

lubricant was

"common practice".

The

QA

inspector

documented

these

observations

in PER951122.

On, August 30,

an

NRC inspector,

during routine reviews of PERs,

conducted

some

followup review of the issue.

The following items were noted

from review of

TVA Specification

G-39, Cleaning During Fabrication of Fluid Handling

Component:

The job required at least class

"B" system cleanliness.

The check valve flanges

were to appear

"metal clean".

The valve flange surfaces

were to be free of oil, grease

and

any other

contamination.

The inspector .further noted that in accordance

with TVA Specification

G-29,

"Standard Haterial Specifications",

specific

and detailed

chemical criteria

for both the gasket

(PF-1060)

and gasket lubricant

(PF-1068)

were to be met

and maintained.

The inspector contacted

the

QA inspector

who initiated the

PER and

was told that any further TVA QA developments

on this issue

would be

passed

on to the inspector.

The inspector,

on. September

14,

1995,

met with

the site maintenance

manager

and

on September

29,

1995, with the site

QA/QC

manager,

and discussed

the issues.

The initial corrective actions for the

PER

failed to fully satisfy concerns

presented

by the site

QA/QC manager

and

was

sent

back for reevaluation.

Pending addi.tional

licensee

action

and inspector

review, this item will be tracked

as IFI 50-260/95-56-02,

Use of Nickel-Based

Thread Lubricants

on Gaskets

in TVA Class

"B" Fluid Systems.

r ~

IS~

~Ii

<gk

One IFI was identified.

4.0

Unit 3 Restart Activities

(37828,

61726,

62703,

37550,

92903)

(Unit 3)

The inspectors

reviewed

and observed

licensee activities involved with the

Unit 3 restart.

This included reviews of procedures,

post-job activities,

and

completed field work; observation of pre-job field work, in-progress field

work,

and

QA/QC activities.

Detailed observation of numerous testing

activities

and other system recovery activities

was conducted.

4. 1

System Pre-Operability:Walkdowns

On September

27,

1995

an inspector

observed

portions of the system

preoperability walkdown of the Sequential

Events, Recording/Annunciation

System.

A pre-walkdown meeting

was .held.

The system engineer highlighted

SSP-12.55,

"Unit 3 System Pre-Operability Checklist" Appendix D,

SPOC

Walkdown

Guidelines,

discussed

previously identified/observed

system discrepancies,

and

noted that the control

room

(CR) emergency

diesel

control panels

were not

within the operability walkdown boundary.

A portion of the walkdown pre-brief

and the actual

walkdown was attended

by the inspector

and

a member of the

licensee's

senior

management staff,

The walkdown was performed

by the team in

a straight-forward, direct

and methodical

manner

and in accordance

with SSP-

12.55,

Appendix

D guidelines.

Haterial condition concerns

were noted

such

as

dirty annunciator

and control cabinet interiors, dirty cabinet filters,

missing cable-tray

covers,

mi'ssing cable

harness '"tie-wraps", cable

harnesses/coverings

in need of replacement.

No major deficiencies

were found.

The post-walkdown meeting

was thorough

and met SSP-12.55

guidance.

The

inspector

concluded that the walkdown was conducted

in accordance

with

approved plant procedures

and in

a thorough manner.

On October

11,

an inspector

accompanied

licensee

personnel

on

a

SPOC

Phase

1

walkdown of the Unit 3 Hain Steam

System.

This walkdown was rescheduled

after

the original September

8,

1995 walkdown was canceled

due to too many

unresolved,

previously 'identified deficiencies

being observed

( IR 95-51).

A

pre-walkdown meeting

was held.

The system engineer,

presented

SSP-12.55,

Appendix D,

SPOC

Walkdown Guidelines

and conducted

an adequate

brief of

previously identified discrepancies.

A portion of the walkdown was attended

by the inspector.

The walkdown was perfor'med

by the assigned

walkdown team in

a direct/thorough

manner

and in accordance

with SSP-12.55

Appendix

D

guidelines.

Host of the material

condition concerns

were minor such

as loose

instrument

panel

bracketing,

loose conduit connectors.

However,

concerns with

outboard

HSIV operation

remained

and were planned to be addressed

prior to the

SPOC

Phase

2 walkdown.

The inspector

found performance of the

SPOC

Phase

1

walkdown to be acceptable

and in accordance

with approved plant procedures.

4.2

Drywell Tour

On September

27,

one of the inspectors

conducted

a detailed tour of the Unit 3

drywell.

The inspector

focused

on the upper elevations

given that fuel load

was expected

in two weeks.

The inspector noted that the reassembly

of

insulation

was progressing well.

The insulation

on the reactor vessel

level

I/i

gl

'g

10

indication reference

leg piping was examined closely

and noted to be in

accordance

with the discussion

in

GE Service Information Letter 470

and in

good condition.

While the drywell was not yet ready for fuel load or startup,

the inspector did not identify any serious deficiencies

in the overall

material condition of the upper levels.

The inspectors

noted that the lower elevations of the drywell will require

considerable effort before they are ready to support startup.

The

inspectors

noted that the recirculation piping wire restraints

were very

loose'nd

questioned if tightening

was scheduled.

A small

amount of trash

was

observed

inside

some ventilation ductwork.

Wedges

were noted

on several

spring cans

on the main steam piping.

The inspectors

also questioned

what

appeared

to be excessive

slack in the cabling running from junction boxes to

the sonic detectors

on the main steam relief tailpipes.

These

items were

discussed

with management.

Some of these

issues

were already in the

licensee's

plans to be resolved.

The licensee initiated actions to address

the remaining issues.

The inspectors

also noted that

an

RHR penetration

contained fibrous .insulation

which ended flush with the drywell interior end of the penetration.

The Unit

3 Restart

Manager indicated that the penetrations

are in the process

of being

walked

down for assessment

of corrective actions.

The inspectors

scheduled

a

meeting with site engineering

personnel

to address

the penetration

questions.

This specific issue will be addressed

as part of the inspector's

review of NRC

Bulletin 93-02 prior to Unit 3 drywell closeout.

The inspector

also verified that the

FME barriers

from the drywell to the

torus were still intact.

At the close of the inspection period,

the licensee

had initiated

a thorough cleanup of the drywell.

The inspectors will continue

to monitor the conditions in the Unit 3 drywell.

4.3

Review of Reactor

Water Cleanup

System

(RWCU) Installed Thermocouple

Modifications

One of the inspectors

performed

a review of the location, setpoint

calculations

and the actuation logic for the newly installed Unit 3

RWCU

thermocouples.

This modification was

made

as

a corrective action to design

and install

a qualified leak detection

system which could detect

and isolate

RWCU pipe breaks

including critical cracks

in the Main Steam Valve Vault,

RWCU

pump rooms

and heat

exchanger

areas.

The modification removed

from service

originally installed temperature

switches

and replaced

them with

thermocouples.

The modification also set in place

a new logic system for

automatic actuation of the reactor containment isolation

and

RWCU system

discharge

valves.

This modification took into account the revised design for

the

RWCU system

implemented

by other

RWCU modifications.

In a related

June,

1993,

NRR evaluation of the adequacy of the Unit 2

RWCU

system line break detection circuitry (Unit 3 is similar),

NRR concluded that

while the

RWCU isolation design did not fully meet

RWCU isolation

requirements, it was consistent with BFN's licensing basis

and was

acceptable.

The

SER also stated that since the

RWCU design relied upon direct

operator action to verify and isolate

a postulated

leak, further verification

~

i

01

11

of operator

information/guidance

adequacy

was necessary.

The inspector

reviewed procedures

and concluded that sufficient operator guidance

was

contained within the following documents:

3-ARP-9-3D

Operator

response

to an

RWCU Leak Detection Circuitry High

Temperature

Alarm/Annunciator (3-TA-69-29)

3-ARP-9-5B

Operator

response

to

an

RWCU Isolation Logic Channel

"A"

High Temperature

Alarm/Annunciator (3-TA-69-834A)

3-ARP-9-5B

Operator

response

to

an

RWCU Isolation Logic Channel

"B"

Hi'gh Temperature

Alarm/Annunciator (3-TA-69-834A)

3-AOI-64-2a Group

3

RWCU Isolation

The inspector

also performed

a walkdown of RWCU pump rooms

and heat

exchanger

areas

and noted location of the installed thermocouples.

The inspector

determined that both the actual detector location

and selected

placement of

the associated

"A C" thermocouples

and

"B D" thermocouples

was adequate,

considering

both actuation logic necessity

and range required for a detection

of thermal

change

in these

areas/rooms.

The inspector

also reviewed the following temperature

calculations for

adequacy of both the calculations

and suppositions:

HD-f3069-920188; Analytical Limits For

RWCU Room Temperature

Isolation

ND-f2069-930032;

RWCU System

Response

to

a Critical Crack Downstream of

the Non-Regenerative

Heat

Exchangers

ED-f2069-890080;

Setpoint

and Scaling Calculations

TE-69-834A-D/835A-

D/836A-D/837A-D/838A-D

Based

on this review, the inspector

concluded that the

RWCU thermocouple

modification was properly implemented.

Thermocouple

placement,

associated

circuitry

and calculations

were adequate

to support Unit 3

RWCU system

operation.

4.4

Flexible Conduit Reviews

On August

17,

1995,

NRR representatives

reviewed information at the site

pertaining to flexible conduit design evaluation.

Among the key items

examined

were: the licensee's

flexible conduit related

commitments,

basis for

categorization

of flexible conduits within the scope of 10 CFR 50.49

and those

belonging. to USI A-46 scope,

basis for licensee's criteria set forth in

General

Engineering Specification

G-40, listing of flexible conduits

evaluated,

results of the licensee's

flexible conduits

walkdown, conduit

separation criteria, basis for determination of the straight line distance

"SD" and

a factor to account for thermal

and seismic displacement

"K,"

documented

engineering justifications for selected flexible conduit outliers,

and the background for the

use of the terminology related to long term vs

interim flexible conduit criteria.

41

i/i

12

The staff performed

a walkdown of several

randomly selected electrical

equipment with newly installed flexible conduits which replaced

those

determined

to be not conforming to the G-40 criteria.

The staff also examined

other randomly selected

equipment with flexible conduits which were judged to

be not conforming to the G-40 criteria, but were technically justified to

remain "as-installed"

based

on case specific evaluation.

The walkdown of

these

items provided

an additional

basis for the staff to conclude that the

licensee

did implement or is implementing

an adequate

and satisfactory

evaluation

program for BFN flexible conduits belonging to both

10 CFR 50.49

and

USI A-46 scopes.

Based

on review of the licensee

submittals related to flexible conduit

criteria for BFN plants,

previous review and acceptance

of criteria used for

resolution of flexible conduit issues

identified in Unit 2 restart

program,

the results of numerous

evaluations

performed

by the licensee for existing

flexible conduit configurations

at the licensee

plants,

the results of design

audit of the licensee's

G-40 criteria and related

engineering

documents,

and

the results of selected

walkdown of several flexible conduit modifications,

NRR has

found that the licensee's

use of the G-40 criteria to eva'luate

the

seismic

adequacy of flexible conduit not connected

to

10 CFR 50.49 electrical

equipment

and within the scope of the

USI A-46 for BFN Units 1,

2 and

3 is

conservative

and acceptable.

Examination of sampled flexible conduit

installations

at the site were satisfactory.

Additional details of the staff's review are

documented

in a safety evaluation

dated

October 3,

1995.

4,5

Unit Separation

Program

During the period of September.

19-22,

1995,

an inspector

reviewed the

activities associated

with the unit separation

program related to the recovery

of Unit 3

~

This program is defined

by procedure

SSP 12.50, Unit Separation

For Recovery Activities.

This has

been

accomplished

by isolating Unit 3

recovery activities

and Unit

1 layup efforts from Unit 2 operational

requirements.

Tagging,

marking, signs,

and color coded drawings

have

been

used to implement these

requirements.

As Unit 3 systems

have

been

recovered

by use of the

SPAE

and

SPOC process,

these

requirements

have

been

removed.

The system engineer

completes

form SSP-161,

Permanent

Removal of Unit

Separative

Boundaries,

to notify site engineering that the boundary isolation

color codings

can

be removed

from drawings.

Once the drawings

are corrected,

Operations

removes

the affected separation

hold order tags,

signs,

tape

and

other markings

from the plant.

The inspector

reviewed procedure

SSP

12.50

and completed

SSP-161

forms.

Twelve of the forms were reviewed.

Several

color coded drawings

were reviewed

in the control

room and

TSC.

No problems

were noted.

The inspector

toured

the Unit 3 reactor building looking for removal of isolation boundaries

and

color coded markings

on unit 3 systems.

In general,

for systems that

had

completed

the

SPOC process

the isolation boundaries

and orange

tape

had

been

removed.

The inspector

reviewed the Unit 3 core spray

system for which the

phase II SPOC

was completed

on September

7,

1995;, and the

EECW system for

which the phase II SPOC

was cqmpleted

June

30,

1995.

The inspector

compared

l

41

13

system

33, service air in Unit 3 and Unit l.

Unit

1 still had the isolation

boundary identified but not in Unit 3.

In general

there

was

a one to one

correlation

between

completed

systems

in Unit 3 and activities for removal of

the separation

requirements.

The inspector discussed

the unit separation activities with a'nit

3 control

room operator.

The operator

was very knowledgeable

on the plans for the

separation

program.

The operator provided

a one

page outline of the

activities in progress

and planned unit recovery activities near completion.

These

plans consisted

of moving out of the separation

program with deletion"of

the separation

requirements.

A revised

procedure

and program would delete the

color coded drawings

and

end

up with a unit separation

program that protects

Units

2 and

3 from Unit 1.

The inspector

concluded that plant personnel

were

well informed concerning

the separation activities.

These activities provided

a controlled

and logical transition coinciding with the completion of Unit 3

recovery activities.

4.6

Unit 3 Reactor

Vessel

Level Backfill Modification

The inspector

reviewed field modifications associated

with W32456A which

installed the backfill system for the reactor vessel

level

system.

A walkdown

of the instruments

and controls

was performed to verify they were installed in

accordance

with the applicable

drawings.

Piping configuration

and labelling

was also verified.

This walkdown identified no discrepancies

with the

installation of these

components.

However,

the inspector identified that.

supports

had not been installed for portions of piping associated

with the

four flowmeters which were required in accordance

with drawing change

authorization

3-47B600-2512-1,

revision 0, detail

B.

Site engineering

was

notified and confirmed that the supports

were required.

Following

installation,

the inspector verified the supports

were installed

as designed.

This issue is discussed

in more detail in IR 95-57.

The inspector

also reviewed the completed post-modification test

package.

This test

was essentially

the

same test performed following the modification

previously performed

on Unit 2.

Although the test

was completed

.

satisfactorily,

one Test Deficiency Was written to document the rapid level

changes

noted

when operating

the condensing

pot shutoff valves 3-SHV-085-0850,

0852,

0854,

and 0856.

The indicated level

swings noted

when the valves were

rapidly opened

were approxi'mately twenty-five inches in magnitude

which was

similar to what was experienced

during the Uni't 2 test.

The Test Deficiency

was dispositioned

by adding

an item to the site tracking system to issue

a

procedure

which will be used to operate

these valves.

Notes or cautions will

be in this procedure to ensure

the valves are operated

slowly and

deliberately.

This .item is. scheduled

to be completed

by Unit 3 restart.

The inspector

concluded that .with the exception of the noted tube support

problem,

the Unit 3 reactor

vessel backfill modification was

implemented

and

tested satisfactorily.

4.7

Unit 3

Eg Program

~I

IR 94-35 documented

a review of the Unit 3

EQ Program Plan.

The

EQ issues

identified in the Unit 2

NRC

SER were addressed

for Unit 3.

The report

concluded that the scope of the Unit 3

EQ Upgrade

had not been

reduced

from

what was accomplished for Unit 2.

The inspectors

review of the Unit 3

EQ

program consisted

of a review of the

EQ equipment in Unit 3 which was not in

the Unit 2

EQ Program.

Additi'onally, selected

EQ

DCNs and

EQ related

emergent

issues

were reviewed.

The following EQ Binders were identified which were

Unit 3 specific:

BFN-3-PENE-003,

GE Electrical Penetration

Assembly

BFN-3-ECON-001

Electrical

Connectors

BFN-3-CABL-052

Anaconda

Cable

BFN-3-CABL-053

ITT Surprenant

Cable

The inspectors

reviewed

EQ Binders

BFN-3-PENE-003,

BFN-3-CABL-052, and

BFN-3-

CABL-053 to determine if they established

environmental

qualification for the

subject

equipment.

EQ Binder BFN-3-PENE-003,

Revision 0,

GE Hodel

F01 Canister Electrical

Penetration

Assembly

was reviewed.

The binder indicated that the

EQ

penetrations

required qualification to the requirements

of 10CFR50.49

and

Nureg 0588 Category

II/DOR Guidelines.

The Binder was prepared

to the

requirements

of procedure

PI-88-11.,

Preparation,

Haintenance,

and Control of

the Environmental Qualification Documentation

Packages

(EQDPs).

The

inspectors

reviewed the documented test data

and verified that it met the

qualification requirements

of 10CFR50.49

and the

DOR Guidel.ines.

The binder contained

two open items, unqualified pigtail connectors

and beta

shielding for drywell side pigtails for

EQ .circuits.

The inspectors

examined

penetration

assemblies

BA and

EC drywell side

and noted that

EQ circuits were

wrapped. with beta tape

and the penetration

assembly

was sealed with foam from

the header plate to the

end of the header

sleeve

per drawing 3-45W803-23

Revision 4.

On the Reactor Building side the inspectors

noted that the

penetration junction box for penetration

BA did not contain

a weephole.

The

work to drill the weepholes for several

EQ junction boxes

had not yet been

performed.

Work Request

WRC294693

had already

been written for this work.

The pigtail wiring was verified to match the field configuration requirements

in the binder.

The inspectors

considered this

EQ Binder to be adequate.

EQ Binder BFN-3-CABL-052, Revision 0, Anaconda. Cable-

TVA Type

HS Signal

Cable

was reviewed.

The binder documented

that the cables

were qualified to the

requirements

of 10CFR50.49

and

Nureg 0588 Category

II/DOR Guidelines.

The

binder,was

prepared

to the requirements

of procedure

PI-88-11

and contained

no

open items.

EQ Binder BFN-3-CABL-053, ITT Surprenant

Cable - TVA Type

HS Signal

Cable

was

reviewed.

The binder was in preparation for initial issue

and documented

that

the these

cables

were qualified to the requirements

of 10CFR50-.49

and Nureg 0588 Category

II/DOR Guidelines.

The binder

was prepared

per procedure

PI-88-

11

and contained

no open items.

0

igl

~~

15

The inspectors

reviewed the test reports

and verified that the test results

met the minimum requir ed performance

requirements.

Applicability of the test

data to the installed cables

was addressed

in the binders.

From review of

these

two binders it was difficult to verify comparison of the test results to

the minimum acceptable

plant performance

requirements.

The minimum tested

insulation resistance

of approximately

lE7 ohms

met the minimum performance

criteria for these

cable types of lE4 ohms.

The licensee

prepared

an

administrative

change to revise the binders

summary section in Tab C/C-6 for

test performance

acceptance.

This was acceptable

to the inspectors.

The inspectors

performed field verification of selected

cables to ensure that

installed cables

met the configuration description

in the

Eg binder

and were

traceable

to the test data in the binders.

The following cables

were

verified:

Anaconda

Cables

(Binder BFN-3-CABL-052)

3PC985-I

Panel 9-54

3PC996-II

Panel 9-55

ITT Surprenant

Cables

(Binder BFN-3-CABL-053)

3PP656

3PP839

Panel

23D

Panel

'23D

The cable types

and cable jacket contract data

matched

the data in the

respective

Eg Binder.

The inspectors

concluded that these

two

Eg Binders

adequately

documented qualification of this equipment to 10CFR50.49

and Nureg

0588/DOR Guidelines

requirements.

The inspectors

reviewed

a sample of Eg

DCNs and performed

walkdowns to verify

that the installed field configuration matched

the design requirements

of the

DCNs.

Field Verification was performed for the following equipment:

3-FCV-74-057

3-FCV-74-059

3-FCV-77-002B

3-FCV-77-0015B

Junction

Boxes

JB0107A and JB0107F

Electrical Penetrations

BA and

EC

DCN W20902A included design

changes

to ensure

environmental

qualification of

valves

3-FCV-74-057

and 3-FCV-74-059.

The changes

implemented

by this

DCN for

3-FCV-74-057 included limit switch compartment

low point T drain,

replacement

of the power terminal block,

and replacement

of the control circuit internal

wiring.

DCN changes

for 3-FCV-74-059 included limit switch compartment

low

point T drain,

removal of control wiring terminal block, replacement

of the

power terminal block, replacement

of the limit switch,

Raychem splices

in the

motor center

taps,

and replacement

of the internal wiring,

The inspectors

verified that the

Eg configuration

changes

had

been

implemented to meet the

DCN requirements.

During the initial inspection,

actuator

3-FCV-74-057

was

oriented

such that the limit switch compartment

T drain was at

a high point.

IQi

i/i

16

The actuator

had

been oriented for HOV testing.

The inspectors later verified

that the actuator

was correctly oriented following completion of the testing.

DCN W17424 contained

requirements for ensuring qualification of the

GE FOI

electrical

penetrations.

This consisted of providing shielding to the drywell

side penetration pigtails.

Raychem

WTBF tape

was installed

on the drywell

side

Eg circuit pigtails

and the penetration

was sealed with foam from the

header plate to overlap the beta tape.

This change

was to prevent post

accident

beta radiation

damage to the drywell side penetration pigtail

insulation.

The inspectors

examined penetration

EC and

BA on the drywell side

and verified that the configuration met the

DCN requirements.

DCN W21813 included design

changes

to ensure qualification for the electrical

components

associated

with valves 3-FCV-77-002B and 3-FCV-77-0015B.

The

changes

consisted

of adding qualified conduit seals

to the existing solenoid

valves,

replacing the limit switches with qualified switches,

and installing

qualified conduit seals

on the limit switches.

The inspectors verified that

the installed field configuration incorporated

these

DCN changes.

The licensee

prepared

work orders to seal

Eg junction boxes with RTV sealant

to prevent moisture intrusion.

Additionally, weepholes

were required to be

drilled in the bottom of the sealed

boxes.

The inspectors

noted that junction

boxes

JB0107A and

JB0107F were sealed with RTV but did not contain weepholes.

The licensee

had

an open work order,

WO 951840302;. which had not been

completed to drill weepholes

in these

and other

Eg junction boxes.

The

inspectors

concluded that the licensee

was adequately

implementing

Eg program

DCNs.

The inspectors

reviewed selected

Eg,related

LERs,

PERs,

and

NRC items to

determine if the licensee

was adequately

addressing

Eg related

emergent

issues.

LER 94-02

was reviewed in detail.

No deficiencies

were identified

and the licensee's

corrective actions

were adequate.

The inspectors

concluded that the Unit 3

Eg program is being

implemented

in

accordance

with the program plan

and regulatory requirements.

4.8

Unit 3 Testing Activities

4.8. 1 Residual

Heat

Removal

System

The inspectors

reviewed portions of the Unit 3 Restart Testing

on System

74,

Residual

Heat

Removal

System.

The testing which was observed

included O-TI-

36A,

RHR Heat Exchangers

Leak Test,

and 3-SI-4.5.B. I.d (I), quarterly

RHR

System

Rated

Flow Test

Loop I.

RHR Heat Exchanger

Leak Test

was intended to determine if the

Loop I

RHR Heat

Exchangers

3A and

3C exhibited leakage

between

the shell

and the tube side.

The inspectors

observed

no increase

in

RHR pressure

on control

room pressure

indicator 3-PI-74-51 with RHR Service

Water pressurized

with an

RHR

SW

Pump

running.

This testing activity was considered

acceptable.

ill

17

quarterly

RHR System

Rated

Flow Test

Loop I was performed per procedure 3-SI-

4.5.8. l.d (I)., The inspectors

witnessed

the flow test of RHR Pump

3A and

verified that the

pump met the acceptance

criteria of > 9000

gpm and

p 125

psig.

Actual observed

values

were

9000

gpm at

175 psig.

The acceptance

criteria of the procedure

met the requirements

of Unit 3 Technical Specification 4.5.B. l.d,

RHR System

Pump Flow Rate.

During the

RHR Pump Rated

Flow Test,

leakage

was noted at

RHR Heat Exchangers

3A and

3C.

The leakage

was determined to be from the shell

side

(RHR) located

at the second

flange from the top, the

RHR boundary flange.

The licensee

initiated work requests

WRC317208

and

WRC286110 to investigate

and repair

3A

and

3C

RHR Heat

Exchanger

leakage respectively.

Work Orders

WO 91-42438-01

and

WO 91-42439-01

were performed

on

RHR Heat

Exchangers

3A and

3B respectively.

The

RHR heat

exchangers

flange bolts were

tightened to the

maximum torque allowed by Procedure

MCI-0-074-HEX001.

The

heat

exchangers

were still leaking.

Engineering

was assigned

the task to

resolve the leakage.

DCN TDCN 38580

was prepared

to evaluate

and repair the

heat exchanger

leakage.

During the

RHR flowrate testing,

the licensee

attempted to perform Loop II

Simulated

RHR Automatic Actuation Test per 3-SI-4.5.B. l.a (II).

An

inadvertent start of the

3C

RHR pump occurred during this testing

due to

a

procedure error.

The operators

secured

the

3C

RHR pump within the

maximum

allowable

3 minute period at minimum flow.

Step 7.2. 11 of procedure 3-SI-

4.5.B. l.a (II) attempted

to inhibit the

Loop II redundant start signal to the

Loop I

RHR pumps

3A and

3C.

The procedure

called for booting contacts

5-6 of

redundant

auto start relays

10A-K25B and

10A-K47B to inhibit the start of RHR

pumps

3A and

3C.

The licensee

determined that the procedure

specified the

incorrect contacts.

A procedure

change

was

made to boot auto start relay

contacts

1-2

and the testing

was completed.

The inspectors

reviewed drawing

3-45E766-21,

Revision

17, Wiring Diagram 4160

V Shutdown Auxiliary Power

Schematic

Diagram,

and verified Loop II redundant start signals to

RHR pumps

3A and

3C were relay

10A-K258 contacts

1-2 and

10A-K47B contacts

1-2

respectively.

The licensee initiated

PER

BFPER951365 to investigate this

procedure

issue.

4.8.2 High Pressure

Coolant Injection System

On September

27,

1995,

an

NRC inspector

observed

the Appendix

R Backup Control

Panel test for HPCI.

The test

was performed using Technical

Instruction 3-TI-

165B.

The purpose of the test

was to demonstrate

control

room electrical

isolation

and remote operability of the

HPCI turbine

steam supply valve 3-FCV-

73-16.

The inspector

observed

the boot inhibiting of relay 23A-K47 and

jumpering of several

contacts

(to prevent

unwanted valve operations

during the

testing).

These

components

were located

on panel

3-9-39 within the Unit 3

Auxiliary Instrument

Room.

Independent verification of these

procedure

steps

was observed.

The specified test

acceptance

criteria were met.

No other test

discrepancies

were identified during conduct of testing.

The inspector

concluded that the restoration activities

and testing of the

Appendix

R Backup Control for HPCI had proceeded

in a controlled manner.

The

ill

igl

i/i

18

test demonstrated

proper control

room isolation

and remote

HPCI turbine steam

supply valve operation.

The licensee's

independent verification of system

test configurations

was adequate.

However, during the test observation,

the inspector

noted significant

accumulation of dust

and lint on electrical

cabinet ventilation filters

located in the Unit 3 Auxiliary Instrument

Room.

The inspector identified

this situation to the licensee

operations fire protection management.

The

inspector indicated that this condition

may reduce cooling air flow to

instruments

during

a time of increased

energizing of equipment

due to restart

activities causing

equipment

overheating

and

a possible fire event.

Licensee

management

initiated corrective action

and the panel filters were cleaned.

On October

11,

1995,

an inspector

observed

operation of the Unit 3 HPCI system

(on auxiliary steam)

in accordance

with HSI-3-073-GOV001,

HPCI Turbi'ne

Overspeed

Trip Test

and Turbine Stop Valve Balance

Chamber Adjustment.

Although several

equipment

problems

delayed the testing, it was later

completed successfully.

A pre-. brief was conducted.

There

was adequate

maintenance

and engineering

personnel

present

to support the testing.

Operations

personnel

were appropriately cautioned

in the operation of the

turbine

and communications

were good.

Operators

used

procedures

when

performing adjustments.

FHE practices

when the overspeed

assembly

access

plug

was

removed

were good.

Two deficiencies

were noted.

During the performance

of step 7.3.26,

valve 3-SHV-73-0707

(governor valve closure booster oil valve

was found to be

6 turns

open instead of the expected I/2 turn open).

After

the turbine

was started, it was noted that the main oil pressure

was indicated

as zero

and the auxiliary oil pump continued to run.

HPCI was tripped

and it was determined that valve 3-RTV-073-0231A was shut

instead of open.

The following day, the inspector

requested

the cause of the

apparently

improperly positioned

valves since the

SPOC

I process

has

been

completed

on HPCI.

After additional

review, the licensee identified that the

73-0707 valve was listed incorrectly'on the OI-73 checklist

as "open".

The

73-231A valve was listed

on Attachment

4 (instrument lineup)

and not reopened.

PERs were subsequently

initiated and portions of the lineup were completed

again.

On October

13,

1995, the inspector

observed

operation of HPCI in accordance

with 3-TI-343,

HPCI Injection Line Flush

and 3-0I-73,

HPCI System.

Auxiliary

steam

was

used to run the turbine.

HPCI piping to and from the

CST was

flushed

and then flow was directed to the vessel

to flush the injection line.

Testing

was delayed initially because

during bypassing of the high water level

trip, incorrect leads

were lifted and it was identified that the turbine would

not trip from CR.

A PER was. initiated to address

that problem.

Subsequently

it was determined that

an incorrect lead

was lifted during the disabling of

the high reactor water level trip function.

During the delay in testing,

the

inspector questioned

CR personnel

regarding the operability of the

HPCI oil

cooler discharge

high temperature

annunciator (3-TA-73-52).

The inspector

had

noted that 3-TS-73-52

was disconnected,

rendering

the annunciator

inoperable.

The switch failed and

a replacement

is being obtained.

CR personnel

were not

aware that the annunciator

would not function,

Compensatory

CR monitoring

actions

were not planned.

Personnel

in the

HPCI room were

aware of the status

if'/i

19

of the alarm

and

a local temperature

gauge

had

been monitored during the

previous

overspeed

testing.

The inspector

noted, that the annunciator

status

was not addressed

during the pre-brief and the

CR panel

window was not labeled

to indicate its status.

It should

be noted that the

SPOC II process

has not yet been

completed

on the

Unit 3 HPCI System.

The above

issues

indicated that status of equipment

during/prior to testing activities was not well controlled.

In the case of

the valves not properly positioned,

an additional

concern

was that the

inspector

prompted resolution of the cause of the deficiencies.

4.8.3 Control Air System/Drywell

Control Air System

.The inspectors

reviewed the licensee's

control of moisture in the control

air/drywell control air systems.

Moisture control

was

by use of desiccant air

dryers in the control air system

and

by refrigerant air dryers in the,drywell

control air system.

The,licensee

performed monthly dewpoint checks

on the

operating air systems

per procedure

O-TI-34, Monthly Control Air System Dryer

Dewpoint Test

and

Purge Control, to monitor air dryer performance.

The procedure

acceptance

criteria for control air required control air

dewpoint at line pressure

to be

<18.

F below outside

ambient dry bulb

temperature

and dewpoint at line pressure

to be

< 35'.

For drywell control

air the procedure

acceptance

criteria required dewpoint at line pressure

to be

<

18 F,below local reactor build'ing ambient dry bulb temperature

and dewpoint

at line pressure

to be

< 39'.

The inspectors

reviewed the following completed

work orders to determine if

the dewpoint test results

met the procedure

acceptance

criteria:

913798600

925863800

931399200

940764200

941803700

941913200

942014400

950051000

950069500

950400100

The inspectors

noted that the work orders

documented test results

which met

the dewpoint acceptance

criteria except for

WO 940764200

where the

2A drywell

control air compressor

dewpoint of 43.7'

was

above

the- 39

F dewpoint

acceptance

criteria.

The licensee

documented

the test deficiency

and

repaired/reset

the refrigerant dryer temperature switch'he retest

which was

documented

in. WO 941242800

was reviewed

and the results

met the dewpoint

acceptance

criteria.

Unit 3 drywell control air samples

were taken after the system

was placed in

service following system flushing activities.

The sampling

was performed in

accordance

with procedure

3-TI-176, Drywell Control Air Sampling.

The

acceptance

criteria was

<

1

ppm hydrocarbon

and

<

1 particle

h

5 microns.

The

results of <

1

ppm hydrocarbon

and 0.2 particulate for both header

samples

met

the acceptance criteria'he

inspectors

reviewed the results of the dewpoint

testing of the Unit 3 drywell control air system after the system, was placed

into service.

The results of the dewpoint checks

met the acceptance

criteria

. ~

Igi

i/i

Igk

20

of procedure

0-TI-34.

The inspectors

concluded that the licensee's

control of

moisture in the control air and drywell control air systems

was adequate.

IR 95-51

documented

an instance

where drywell control air compressor

38 local

control station handswitch,

3-HS-032-0067

was found in the

AUTO position while

a tagout required it to be in the

OFF position.

The switch is located

in an

area

where it is subject to being

bumped

and inadvertently mispositioned

by

personnel traffic.

The inspectors

noted that

a guard

had

been installed

on

the switch to prevent further mispositioning.

4.8.4 Hain Steam Isolation Valves

On October

1,

1995,

the inspector

observed

portions of surveillance test 3-SI-

4.7.D. l.a-3,

Hain Steam Isolation Valves Closure

Time Test.

The testing

involved the stroking of the Outboard

HSIVs only.

During the testing

evolution,

a number of minor procedural

deficiencies

were encountered

as the

procedure

was being performed for the first time on Unit 3.

These

deficiencies

were noted

and documented

appropriately.

A more significant

problem was discovered

during the cycling of MSIV 3-1-27.

When the operator

attempted

to open the valve,

no valve movement occurred.

The operator

stopped

the test to investigate

the problem.

The investigation revealed that

an air

supply valve, 3-32-2586,

was closed in lieu of the required

open position.

Upon further discussions

held within the control

room and personnel

at the

HSIV, it was determined that the valve in question

(3-32-2586)

had

been

closed

the previous

day due to

an air leak in the vicinity.

The repositioning of the

valve was not documented

in the system

32 (Control Air) status

log as required

for a system that

had previously undergone

SPOC

Phase I.

The Unit 3

SRO had

assumed

that because

plant maintenance

personnel

were

aware

of. the air leak,

a

work order would be initiated

and clearance

would be placed

on the valve to

facilitate the repair.

This is the second

example of an instance

where status

control

was not being rigorously maintained

on

a Unit 3 system that

had

undergone

the

SPOC

1 process.

Paragraph

4.8.2 describes

two HPCI

instrumentation

valves which were found incorrectly positioned during testing.

Neither of the systems

have

been declared

operable

at the time the issues

were

noted.

The residents will continue to monitor the licensee's

progress

in this

area.

4.8,5 Reactor

Core Isolation Cooling

On October 9,

1995,

the inspector

observed

portions of the performance of 3-

SI-4.2.B-40A,

RCIC System Logic Functional Test.

The procedure

was performed

in a satisfactory

manner with minor procedural

deficiencies,

such

as

typographical

errors

and

a reference

to

a wrong fuse number; dispositioned

in

an appropriate

manner.

The procedure

demonstrated

that the

RCIC system would

automatically restart

on low reactor water following a trip on high level

as

required

by THI action item II.K.3.13.B.

On September

30, the inspectors

observed

portions of overspeeed

testing of the

RCIC system

on auxiliary steam.

Although several

delays

occurred

due to emergent

equipment

problems,

corrective actions

were completed

as required

and

no deficiencies

were noted

involving conduct of the testing.

No violations or deviations

were identified.

IS~

~(

~gi

21

4.9

Corrective Action Tracking Documents

On September

11,

1995,

the licensee

submitted

a letter to the

NRC which

documented

the current status of the Unit 3 CATDs.

In letters

dated

September

5,

1995

and January

18,

1995, .the licensee

had previously explained that

intentions

were to pursue

completion of corrective actions for all Unit 3

CATDs prior to Unit 3 return to service.

The Unit 3 "open"

CATDs have

been

"rolled over" into NCOs

and tracked in TROI like other open issues.

IR 95-10

and 95-26 documented

NRC inspection of the process

used for rollover and

closure of the

CATDs.

Numerous

NRC inspections of CATD corrective actions

have

been

completed

over

the last year.

Frequently,

CATDs were reviewed during

NRC inspection of

related technical

issues.

The inspectors verified that actions

were completed

and in most cases

checked that the original concern

was addressed

adequately.

No significant discrepancies

were identified during any of these

reviews.

The

licensee's

review and closure of the corrective actions for CATDs have

been

extensive

and conservative.

The September

1'1,

1995 letter stated that corrective actions for eleven

CATDs

are not expected

to be completed prior to Unit 3 return to service.

Return to

service in this correspondence

is defined

as criticality which is currently

scheduled

for the middle of November.

The eleven

open issues

can

be divided

into the following categories:

Six are pending resolution of USI A-46 issues

which are currently

scheduled for Harch

19,

1996.

Two involve personnel

safety issues

(rigging) associated

with Hain Steam

Relief valve removal/reinstallation.

One is connected

to the security upgrade project (security lighting

drawings)

which is expected

to be completed

in January

1996.

One involves potential

inleakage

to the Control

Room Emergency

Ventilation Syst'm (question of GDC 19 compliance).

This issue is

pending additional

NRC review and is expected

to be resolved

by February

29,

1996.

In

a letter dated

Harch

19,

1993,

the

NRC stated that the

licensee

had adequately

addressed

each of the staff's concerns

at that

time,

Additional

NRC review is being conducted

regarding details of the

dose calculations.

One is pending inspection of feed

pump minimum flow lines for excessive

vibration.

The lines will be checked during feed

pump operation.

Corrective actions

are scheduled for completion

by January

3,

1996.

The inspector

concluded that these

open corrective actions

do not represent

significant deficiencies

which would preclude restart.

The majority of the

incomplete actions

are pending completion of extensive

longterm projects.

The

inspector

reviewed the status of open

items associated

with CATDs.

As of

October 6, there

were approximately

30 open

items that

had

CATD actions

associated.

The licensing manager is tracking resolution of these

items

~

i

)0(

~i

22

closely.

Although several

large

scope

(program issues)

CATDs remain to be

closed close to startup,

the inspector

concluded that the schedule of CATO

corrective action completion is attainable.

Based

on the

NRC inspections

which

been

completed

on the

CATDs with positive results,

and this review of the

remaining

open actions,

the inspectors

concluded that the Unit 3

CATDs have

been

adequately

addressed

by the licensee.

The number of incomplete

CATD

corrective actions

on Unit 3 at restart will be significantly lower than the

corresponding

number

open at Unit 2 restart.

4. 10

Nuclear Performance

Plan Issues

During reviews last year to ensure that all potential safety issues

wer e

scheduled

for inspection prior to Unit 3 restart,

the inspectors

noted

two NPP

items which appeared

to be not specifically addressed

by any other open items.

The two subjects

were

HPCI governor controls

improvements

(page

IV-17) and

resolution of open Corrective Action guality Reports

(page II-58).

The inspector

reviewed

NRC documents

and did not identify any specific

regulatory concerns

involving the

HPCI governor control

system.

From review

of licensee

documentation,

the inspector determined that

a

1986 task force had

developed

a list of HPCI improvements.

The list consisted

of numerous

modifications.

DCN W23730A involved modification of the electro-hydraulic

controls

intended to improve governor valve response

and reduce

the overspeed

transient

on HPCI starts.

Other

HPCI improvements

were included in

DCN

W17834A.

The inspector

reviewed SILs 336,

351

and

480 to gain additional

understanding

of HPCI operations

and testing.

The inspector

reviewed the packages

for DCNs W23730A and

W17834A and verified

that selected

testing listed

on the

SSP-121

form had

been completed.

The

inspector

examined

the

new

EG-H control

box and

ramp generator/signal

converter.

The model

numbers

matched

those

in the modification documentation.

Selected

conduits

and wiring connections

were verified to match the

DCAs.

The inspector

walked

down the control oil piping and verified that the

installation matched

the drawings

and the changes

describ'ed

in the

modification had

been

completed.

The inspector identified that the details

section of drawing 3-47E812-2

(CCD flow diagram of HPCI oil system)

did not

match the installed configuration.

Two oil lines between

the

EG-R and the

remote

servo were not connected

as

shown.

A licensee

engineer verified that

the drawing was in error and that actual installation

was correct.

Potential

Drawing Discrepancy

95-501

was initiated to address

the identified problems.

One minor labeling error was also noted

and reported for correction.

As described

in paragraph

4.8.2 of this report,

HPCI was operated

on October

11

and

13,

1995

on auxiliary steam.

The overspeed trip was successfully

tested

and flow was injected into the reactor vessel

to flush the injection

line.

During these

operations,

the

HPCI governor

system

appeared

to operate

properly.

PERs

951485

and

951486

and 951486 were initiated on October

12 to

address

problems involving the governor system.

PER 951486

addressed

problems

with the

ramp generator

and signal converter.

Defective parts

and assembly

problems

were identified on parts

drawn from supply.

Additionally, the spares

were apparently

not periodically energized

as the vendor storage

instructions

IO~

ig>

Igi

23

recommended.

Failure to properly store

spare

EG-N parts

has

been recognized

by other utilities as

a cause of failures.

In 1994,

the resident

inspectors

had questioned

the licensee

on

EG-N parts storage

practices

and received

information indicating that the

EG-H components

are properly controlled in

storage.

PER '951485

was initiated by the system engineer

and addressed

deficiencies

in the

HPCI governor controls calibration procedures.

Recommended

corrective action include revision of the procedures.

HPCI has not yet been

through the

SPOC II process

or declared

operable.

Resolution of both

PERs wi.ll be tracked

as part of the

HPCI system recovery

processes.

The inspector

concluded that the governor control modifications

have

been

completed

in accordance

with the

DCN packages.

This item is closed

for Unit 3 restart.

The inspectors will continue to monitor HPCI system

testing.

The other

NPP item involved unresolved

Conditions Adverse to Quality Reports

(CAQRs).

In the past,

TVA did not always take timely action to resolve

CAQRs.

The Licensee

has shifted to

a Problem Evaluation Report

(PER)

program for

corrective actions.

The

PER program continues

to be refined

and

has replaced

most of the various deficiency reporting

systems

onsite.

The

PER program is

.inspected

on

a continual

basis

by the resident

inspectors.

While some

weaknesses

have

been

noted in the past,

overall the

PER program

has

been

an

effective corrective action program.

Unresolved

CAQRs (earlier deficiency

reports

were consolidated

into CAQRs) are being tracked in TROI for

resolution.

As stated

on

Page II-58 of the

NPP, prior to restart of Unit 3

any unresolved

CAQRs will be evaluated.

NRC reviews of the license's

tracking

systems

throughout the Unit 3 recovery

have not identified any significant

deficiencies.

5.0

Review of Open

Items

(92700)

(92901)

(92902)

(92903)

(92904)

(TI2515/65)

The open

items listed below were reviewed to determine if the information

provided met

NRC requirements.

The determinations

included the verification

of compliance with TS and regulatory requirements,

and addressed

the adequacy

of the event description,

the corrective actions

taken,

the existence of

potential generic

problems,

compliance with reporting requirements,

and the

relative safety significance of each

event.

Additional in-plant reviews

and

discussions

with plant personnel,

as appropriate,

were conducted.

5. 1

(CLOSED)

GL 88-14,

Instrument Air Supply Problems Affecting Safety-

Related

Equipment (Unit 3).

As presented

in IR 95-38,

most items for this

GL were closed.

The issue

remained

open pending

checks of equipment operability, performance of

functional testing,

and related

system

AOI revision completion.

The inspector

reviewed the remaining

issues

and observed/noted

the following:

.Drywell air quality testing

was performed

on September

15,

1995

and'esting

results,

received

October

5,

1995,

were satisfactory.

System

AOIs were revised

and noted

as complete

on August 9,

1995.

IQi

~I

if'

24

System

components

were satisfactorily tested for their failure to an as-

designed

position

on August 29,

1995.

HSIV/ADS accumulator periodic leakage test procedure validation has

been

scheduled

as part of the main steam

system

component testing

package.

Satisfactory

main steam

system testing will complete validation. of these

procedures.

Based

on the inspector's

specific review of Unit 3 system operability and

reviews of the AOIs and related

documentation,

GL 88-14 is closed for Unit 3.

5.2

(CLOSfD) THI Action Item II.F.1.2.E

(Formerly II.F. 1.5) - Suppression

Pool/Containment

Water Level Honitor (Unit 3).

IR 95-31 describes

review of many of the elements

of this item.

The issue

remained

open pending

equipment calibration/testing

inspections,

instrumentation

string functional testing,

and following approvals of

associated

level

component testing,

maintenance,

and operating

procedures.

An

inspector

reviewed/observed

closure activities for the remaining issues

and

.noted the following:

Instrument string testing for torus accident level monitoring strings

(PT/PI/XR-64-159A

& 159B)

was performed October

12

& 13,

1995.

Tests

were performed in accordance

with Procedure

3-SI-4.2.F-20(A)

and 20(B),

Suppression

Chamber Water Level - Wide Range.

The inspector

reviewed the

test results

and concluded

they were satisfactory.

System

component operating instructions

were presented

to the licensee's

PORC

and approved for use

September

6,

1995.

"A" and "B" train component test procedures

were presented

to TYA's

PORC

and approved for use in June,

1995 for the A-train level instrument

and

April, 1995 for the B-train level instrument.

The remaining TI2515/65 items were confirmed to have

been

adequately

addressed

by the licensee.

Based

upon;

1) the

above

items,

2) examination of related

component

procedures,

3) evaluation of modification documents

and 4) review of

operability involving the Unit 3 torus water level monitor,

THI Action Item

II.F.1.2.E, (II.F.1.5), is closed for Unit 3.

Also, during the

above October 12-13,

1995 observations

of the instrumentation

testing,

the inspector walked

down various portions of system piping such

as

test

stand tubing

and instrument

sensing lines.

During the walkdown, the

following was noted:

Tubing/piping was secured

properly

and with allowance for adequate

seismic restraint.

Sensing

portions for system instrumentation

were adequate

and routed

properly for proper detection function.

lpga

25

System modifications were

made in accordance

with design

slope

and

desired piping/tubing run.

Hodification line sl'ope was, for the most part, positive,

and

any

required negative

slope

due to support structure interference

was held

to

a minimum.

During the above

walkdown and during testing for assurance

of meeting the THI

Action Item,

an examination of instrumentation line slope

was performed

by the

inspectors.

The inspectors

noted that in

NRC IR 94-24,

a detailed

examination

of HPCI instrumentation line slope

was previously performed.

The inspectors

reviewed results of a February,

1995,

gA "vertical slice" of reactor

vessel

level

(RVLIS) instrumentation.

PER 950136

was initiated to address

questions

raised during review of this RVLIS line slope

and the inspectors

studied the

completed

PER.

The inspectors

concluded that instrumentation line slope

on

Unit 3 safety

systems

has

been

adequately

addressed

by the licensee.

The

Instrument

Sensing

Line Slope

Program is closed.

5.3

(CLOSED) IFI 84-32-02,

Unit 3 Torus Narrow Range

Level Instrumentation.

As presented

in IR 95-31,

IFI 84-32-02, detailed the "greater than allowed by

Unit 3 Technical Specification" difference in indicated level

between

narrow

range indicators

LI-64-54 and LI-64-66.

Significant review of this

modification had

been

completed;

however, this item remained

open pending

review of instrument testing/calibration

and

upon

a check of component

operability.

Reviews were also required

on performance of functional testing

and completion of changes

to related plant maintenance/testing

and operations

procedures.

Instrument testing for the level monitoring string,

(PT/PI/XR-64-

66)

was performed

on October

13,

1995

and test results,

received

October

14,

were satisfactory.

Based

on these

reviews,

IFI 84-32-02 is closed for Unit 3.

5.4

(CLOSED) Generic Safety

Issue

(GSI)

41

and Hulti-Plant Action (HPA) Item

B058/TAC H51014;

BWR Scram Discharge

Vol,ume System (Capability Issues).

The inspector

reviewed the August 17,

1993

TVA to

NRC letter,

and verified the

following Unit 3 Scram Discharge

Volume

(SDV) modifications

had

been

completed:

The

SDV has

an independent,

closely-coupled,

scram discharge

instrument

volume (SDIV).

The vent lines are cross-tied

and contain

vacuum

breakers.

System vent/drain lines

have series isolation valves

and

an originally

installed drain piping relief has

been

removed.

The

SDIV has

two main control

room alarms

"volume not drained"

and

"CRD withdrawal inhibit" alarms.

With SDIV accumulations

of

approximately

50 gallons of water,

a scram signal is initiated.

A diverse

mix of float switches

and sealed differential pressure

transmitters/

switches

had

been installed in the original modification;

lpga

26

but the differential pressure

transmitters

were replaced with

transmitters

with heated

reference

RTDs.

As presented

in

a May 11,

1995

TVA to

NRC letter,

the float switches,

while acceptable,

presented

a slow scram input response

(about

20

seconds);

Therefore,

TVA has decided to retain the originally installed

scram pilot air header

low pressure

switches

due to concerns

regarding

SDV fill-up rates

versus float switch scram signal

response

delays.

As noted in a September,

1993 analysis of BFN's SDVs/SDIVs,

a successful

scram

would be achieved without the scram pilot air header

low pressure

switches,

provided that the

CRD stall flow rate

and the

SDV water level instrument

response

characteristics

remained within acceptable limits.

However,

since

performance of this analysis,

BFN has

noted "higher than expected"

Unit 2

CRD

stall flow rates.

BFN also noted that the flow rates

could preclude long-term

conformance of having adequate,

"within acceptable limit", SDV capacity.

Thus,

as stated

in an April 27,

1995

TVA letter to the

NRC, the licensee

determined that their most prudent

course of action would be to maintain the

scram pilot air header

low pressure

scram function.

In June,

1995,

a design

change

(OCN) was

implemented

on Unit 3 and

OCN completion resulted

in

installation, of qualified /nit 3 scram pilot air header

low pressure

switches.

On June

30,

1995,

TVA submitted

proposed

TS amendment

359, which made

reference

to and

added this scram function.

In March,

1987,

a regional

NRC inspector

reviewed actions

taken

by TVA/BFNP in

response

to Generic Safety Evaluation Report,

"BWR Scram Discharge

System

Safety Evaluation",

IR 87-13.

The inspection

was performed to verify actions

taken to bring all of the

BFN units into compliance with guidelines

establ.ished

by the Generic

SER on

BWR SDV systems'o

violations or

deviations

were identified.

The inspectors

performed

SDV system

walkdowns

and reviewed applicable Unit 3

documentation

including; TI 2515/90,

"Inspection of Licensee

Implementation of

MPA-58,

SDV Capability",

a TVA to

NRC letter,

dated April 27,

1995,

and

IR

87-13.

The following observations

were made:

The Unit 3

SDV headers

are sized in accordance

with

GE OER-54.

The

headers

are hydraulically coupled to the

SDV instrument

volumes in such

a way which permits

oper ability of the instruments prior to

a loss of

system function.

Unit 3

SDV level instrumentation

is provided which allows for an

automatic scram, while sufficient volume exists in the

SDV.

Instrumentation

taps

are provided

on the vertical instrument

volume

and

not on connected

piping.

Scram instrumentation

is currently capable of detecting water

accumulation

in the instrument

volumes.

This instrumentation

provides

both diversity and redundancy.

IQi

~I

i/i

27

Unit 3

SDV vent

and drain functions appear

not to be adversely affected

by other system interfaces

and the

SDV vent

and drain valves

are

designed

to close

upon loss of air/power.

Unit 3

SDV instruments

are provided which aid the operator prior to any

scram initiation.

They provide detection of water accumulation within

the instrumentation

volumes.

A single active failure will not defeat the isolation of the Unit 3

SDV

vent

and drain valves.

As with the currently operating Unit 2

SDV system,

Unit 3 quarterly testing

will be performed to ensure that:

Vent and drain valves are periodically tested

and that valve closure

times are less

than

30 seconds.

" In-place" level detection

instrumention is periodically tested.

Overall

SDV system operability is periodically tested

and at least

once

during each operating cycle of Unit 3.

This quarterly test,

using Unit 3 SI, 3-SI-4.3.F. l.b,

"SDV Valve Operability

SI", for guidance is performed

by simulating

a scram signal to the

SDV drain

and vent air pilot valves

3-FSV-85-37A and

37B using test switches

located

on

the Unit 3 Auxiliary Instrument

Room Panels 9-15

and

17.

A chart recorder is

connected

to each drain

and vent valve "closed" indicating switch to allow

testing of all valves simultaneously to ensure

they close in the specified

time limit of less

than or equal

to 30 seconds.

Provisions

have

been

made for

testing using

a stop watch in lieu of a chart recorder,

although

use of the

chart recorder is preferable.

This SI will also

be performed

immediately

following discovery of an inoperable vent/drain valve

and weekly thereafter,

until the valve is declared operable'nit

3 personnel will also perform

monthly

SDV vent/drain valve position verifications using Unit 3 Surveillance

Instruction (SI), 3-SI-4.3.F. I.a,

"SDV Valve Open SI".

On September

29,

1995,

TVA instrument maintenance

personnel

experienced

problems with testing/calibration of the Unit 3 SDV/SDIV instruments.

It was

determined that

a "hydrolasing"

and flush of the system

was desirable

and

on

October 4,

1995,

per

WO 18186-01,

a cleaning of the system

was performed.

Flush sludge deposits

from the both the

SDVs

and

SDIVs were of a "charcoal"

color and consistency

which was of the

same

sludge color and consistency

as

that observed

from a flush of the Unit 3

HCUs performed earlier in the year.

After a thorough flush of the system

and after observance

of clear flushing

water,

on October

7,

1995,

system piping end covers

were reinstalled.

One of

the inspectors

observed

torquing of some of the end covers.

gC personnel

were

present

and knowledgeable

regarding

the torque requirements.

On October 7,

the system instrumention

was reinstalled

and calibration of the instruments

was subsequently

completed.

Based

on these

reviews,

both

GSI

41

and

HPA B-58, is closed for Unit 3.

lgi

ig>

Igl

28

5.5

(CLOSED) TI'515/121

(GL 89-16), Verification of Mark I Hardened

Vent

Modifications - Unit 3

As presented

in IR 95-38, significant review of this TI has

been

performed.

The item remained

open pending review of system testing/verification of an

associated

EOI. Inspectors

reviewed remaining issue closure activities

and

observed

the following:

System functional testing

was performed

on September

17,

1995.

Testing

indicated that the current Unit 3 vent path will perform its function.

The associated

system

EOI, 3-EOI Appendix 13,

"Emergency Venting Primary

Containment,

was approved for use

on October

13,

1995.

During

a walkdown.,

an

NRC inspector

noted that

an associated

Unit 3

system valve pit, located outside the reactor building,

was not fully

secured

by bolting as directed

by system drawing/design.

Accompanying

licensee

personnel

stated that this valve pit would

be. adequately

secured

and sealed prior to Unit 3 operation.

This was confirmed

by the

inspector

on October

11,

1995.

Based

upon the

above

and

an inspector's

specific review of the Unit 3 hardened

vent system operability, the associated

EOI,

and other related

TI/GL

documentation,

TI2515/121

(GL 89-16) is closed for Unit 3.

5.6

(CLOSED) (Unit 3)

LER 50-259,

260, 296/91-15,

HPCI

Low Suction Pressure.

The licensee's

actions to address

this issue

had

been

inspected

as described

in IR 95-10.

The item remained

open pending observation

of testing.

On

October

13, the Unit 3 HPCI system

was operated

(on auxiliary steam)

in

accordance

with 3-TI-343,

HPCI Injection Line Flush

and 3-0I-73,

HPCI System.

The testing is further described

in paragraph

4.8.2 of this report.

No

problems

were noted involving .the suction low pressure circuitry.

The

inspector verified that the low suction pressure

switch had

been calibrated

and tested

(procedure

LCI-3-P-73-029).

The setpoint listed

in. the

CR

annunciator

response

procedure

matched

the setpoint listed in the calibration

procedures.

Based

on this review and the observed

HPCI operation,

this item

is closed.

5.7

(Closed)

TMI Action Item II.K.3.28, gualification of ADS Accumulators.

This action item involved two concerns

related to the qualification of the

ADS

accumulators.

The

ADS system for Unit 3 consists of six pneumatically

operated

SRVs each with an accumulator

and check valve.

The accumulators

have

an approximate

volume of one gallon

and are normally supplied

by the drywell

control air system.

The first concern dealt with the short-term (six hours)

operability of the accumulators

and their capability to cycle the valves

open

five times at design pressure.

The

NRC staff determined that the Browns Ferry

ADS accumulators

met this criteria

as described

in

a

NRR Safety Evaluation

dated July 24,

1985.

'

i,

i/i

~k

29

The second portion of this action item dealt with the long-term (100 days)

functionality of the

ADS accumulators.

To meet this criteria, the licensee

implemented

a design

change

which utilizes the

CAD system

as the backup supply

for air to the drywell control air system which in turn pressurizes

the

ADS

accumu'lators.

Additionally, the drywell control air system

was separated

into two trains within the drywell.

The inspector

reviewed portions of the

design

change

(W17937),

reviewed the applicable drawings,

and walked down

portions of these modifications to ensure

these criteria were met.

Plant

procedures

3-AOI-32A-1 (the abnormal

operations

procedure for loss of drywell

control air)

and 3-0I-84 (Containment Atmospheric Dilution system operating

procedure)

were also reviewed to ensure

appropriate

and technically sound

operating instructions

were in place to allow for connecting

the

CAD system to

the drywell control air system.

During the procedure

review,

a number of

labeling deficiencies

were noted

by the inspector.

Plant operations

personnel

indicated that these

matters

would be corrected.

Lastly,

a number of the post

modification tests for this design

change

were reviewed.

The

PMTs reviewed

were

as follows;

(1) 3-SI-4.7.G. l.a-l, Containment

Atmospheric Dilution

System Valve Operability and

(2) 3-SI-4.7.A.2.g-3/84a,

84b,

and 84d,

Primary

Containment

Local

Leak Rate Test

Containment Atmospheric Dilution-

Penetrations

X-25 and X-205.

Based

on this review of the licensee's

actions,

this item is closed.

5.8

(Closed)

THI II.K.3.13.B, Separation

of High Pressure

Coolant Injection

and Reactor

Core Isolation Cooling System Initiation LevelsAnalysis

and Implementation

This action item involves two separate

issues.

The first portion of this item

dealt with the separation

of HPCI

and

RCIC system reactor water level

initiation setpoints.

In relation to this matter,

the licensee

endorsed

the

BWR Owners

Group evaluation

(performed

by General

Electric) which stated that

the separation

of HPCI

and

RCIC initiation levels would be of negligible

safety benefit.

The staff endorsed this position in

a Safety Evaluation dated

March 16,

1983.

The second portion of this item deals with the restart of RCIC on

a low

reactor level condition following an automatic shut-off on high water level.

In order for the

RCIC system to be able to automatically restart

in the

above

described

manner,

a modification to the

RCIC control logic was performed in

accordance

with DCN W17534A.

Nore specifically, this design

change

was

implemented

by altering the valve which closes

on

a high level condition.

Prior to the modification, the turbine trip valve (3-FCV-71-9) would close

on

a high water level.

Following the modification, the steam supply valve (3-

FCV-71-8) will receive the close signal

on

a high level condition.

Other

RCIC

trip signals will continue to close the turbine trip valve

and require

manual

action to reset

the system for injection.

The inspector

reviewed portions of

the design

change to confirm these

changes

were covered.

In addition,

the inspector

reviewed 3-0I-71, the Unit 3

RCIC System Operating

Procedure,

to ensure this change

in operating

methodology

was recognized.

The

plant licensed

operator training manual for the

RCIC system,

OPL171.040,

was

also reviewed

by the inspector to ensure this restart feature of the system

was acknowledged.

Finally, the inspector

observed

portions of the

PHT, 3-SI-

0

i/i

i/i

<gl

30

4.2.B-40A,

RCIC System Logic Functional Test, to ensure that the system would

automatically reinitiate

upon receipt of low level signal following a high

level condition.

Based

on this review of the licensee's

actions, this action

item is closed for Unit 3.

5.9

(OPEN) IFI 50-260/95-41-01,

EDG lA Turbocharger

Inspection.

In preparation for the restart of Unit 3, the licensee

contracted for an

independent

Operational

Readiness

Review Team to assess

the readiness

of the

station to begin multi-unit operations.

One of the issues

reviewed

by the

ORRT was the failures of the

1C and

3A

EDG turbochargers.

Several

NRC

inspections

have

been

conducted

on the failures.

While performing this

review, the

ORRT noted that

a vendor "modernization

recommendation"

for a pre-

lubricating system

had not been installed

on the Browns Ferry

EDGs.

In

addition, of the approximately

84

EMD EDGs currently being utilized in this

capacity at nuclear

power plants in the United States,

only the Browns Ferry

and

one other licensee's

EHD EDGs have not had this modification installed.

The

ORRT concluded that the licensee's

documentation

of the issue did not

adequately

address

these specific questions

adequately.

The resident

inspectors,

when informed of the ORRT's concerns,

concluded that additional

NRC review of the issue

was warranted.

On October

11,

1995,

a teleconference

was conducted

between

the licensee

and

the

NRC (Region II, NRR,

and the Resident

Inspector Office) to discuss

the

status of the licensee's

corrective actions related to the

1C and

3A

turbocharger failures.

During the teleconference,

the licensee

explained that

they

had determined that the pre-lube modification was not required to be

implemented

due to the methodology in which the engines

are operated.

Hore

specifically, this change is only of benefit to an engine which is fast

started

during

a period from 15 minutes to

3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> from which it was last

operated.

Because

the licensee

procedurally prohibits operation of the

EDGs

in this manner,

the vendor concurred with the licensee's

decision not to

implement the modification.

Additional actions

being taken

by the licensee

are

as follows;

1) The

licensee

has

purchased

two sets of new turbocharger

gears

which will be

metallurgically examined for manufacturing defects.

2) Recently,

the licensee

discovered

two planetary

gears

from the

3A turbocharger

which failed on August

24,

1992.

These

gears will be sent to TVA central

laboratory for analysis.

3) In June,

1996,

the licensee will remove the

1A turbocharger for destructive

examination.

This effort will be accelerated if the testing of the

above

mentioned

gears

demonstrates

a manufacturing

problem.

The inspectors will

continue to monitor the licensee's

corrective actions related the past

turbocharger failures.

Based

on this review, this item will remain

open

pending final resolution of this matter.

5. 10

(OPEN)

VIO 260,296/95-31-01,

Core Spray Testable

Check Valve Testing

not in Accordance with Requirements.

guestioning

by

a

NRC inspector during observation of testing led to the

'dentification

that the

CS testable

check valves

were not being tested

in

accordance

with the approved

IST program requirements.

The disk was not being

~

~

ii

<5>

Igi

31

cycled fully open

and the procedure for setting the disk position indication

lights was not sufficiently detailed.

Additional review of this issue is

documented

in IR 95-43.

On August 30,

1995,

one of the inspectors

observed

cycling of 3-FCV-075-0054 (with the air actuator)

with the top cover removed.

Maintenance

personnel

set the disk position switches

using

a revised

procedure.

The inspector

concluded that the disk position indication lights

were set to more accurately reflect disk position.

The inspector

observed

that the disk initially slammed fully open

when the actuator

overcame

the

small force present

when the disk was fully shut.

The disk could be easily

opened

from the actuator

end of travel position to fully open.

The inspector

noted that the

AUO involved deliberately verified (by,reading

the valve label)

that

he was operating

the correct

component

before opening the valve.

Subsequent

to these activities, the valve failed local leakrate testing

and

additional

work was performed

on the valve.

After this work was completed,

the valve was stroked fully open using

a torque wrench.

The inspector

reviewed the data for the manual

stroking of both Unit 3

CS testable

check

valves.

WOs 95-12395-0

and

12445-0 indicated that the

maximum torque required

to fully open the disk was

30 ft-lbs.

This value is significantly less

than

the pressure

that would be applied if CS .flow was initiated.

The inspector

concluded that the Unit 3 valves

had

been satisfactorily stroked

open.

This

item is considered

addressed

for the Unit 3 restart.

On September

15,

1995

the licensee

submitted relief request

PV-37 which addressed

alternate

testing

of the

CS check valves.

The violation remains

open

pending

NRC review of the

licensee's

submittal

and stroking of the Unit 2 valves.

5. 11

(CLOSED)

LER 259,

260,

296/94-02,

Raychem Tubing for

EQ Applications

On October 31,

1994, during installation of Raychem heat shrink tubing, the

licensee

discovered that WCSF-070-N shrink tubing from lot no.

15057 would not

'hrink down enough to form a proper seal for LOCA harsh

environment

applications.

The licensee

placed the inventory of WCSF-070-N tubing from lot

no.

15057

on

QA hold on October 31,

1994.

The allowable range for

EQ

applications for WCSF-070-N was 0.07 to 0. 14 inches diameter

.

The material

was procurred

on

TVA procurement

document

21042-E19060Q

item

6 and

was stocked

as

TVA item BGN673K.

On November

1,

1994,

TVA sent

samples of WCSF-070-N tubing from lot no.

15057

to Raychem for evaluation.

The

Raychem written response

indicated that this

material. did have

a reduced

shrinkage

and could only be used for LOCA harsh

environment application for a range of .081 to

. 14 inches diameter.

Material

which had

been

issued to the field and

had not been

used

was returned to the

warehouse

and placed

on

QA hold,

TVA could not determine

a definitive root

cause

but suspected

manufacturing

process

problems

because

no other tubing

from different lots had exhibited this problem.

TVA determined that

no tubing of this lot no.

was

used in 10 CFR 50.49

applications

on Unit 2.

All WCSF-070-N tubing from lot no.

15057

was returned

to Raychem.

The licensee's

review indicated that only 4 cases

were identified

where

WCSF-070-N tubing from lot no.

15057

was

used

on Unit 3.

The

applications

were

uses

as

shims where the tubing is shrunk

on

a cable

and

another

piece of shrink tubing is installed over the joint.

The four

I

.0"

if'/i

ill

32

applications

were identified to fall within the reduced

range of .081 to

. 14

inches for which Raychem stated that lot no.

15057 would remain acceptable.

The inspectors

reviewed the correspondence

from Raychem

and confirmed that the

vendor indicated that the lot was acceptable if used within the range of .081

to

. 14 inches diameter.

The field verification data

sheets

for Unit 2 in

Eg

Binder BFN-O-E(-SPLC-OOI, Revision

15,, were reviewed

and the inspectors

confirmed that

no WCSF-070-N tubing from lot no.

15057

was installed in

Eg

applications

on Unit 2.

The Unit 3 field verification data sheets

had not yet

been

incorporated

into this binder.

This issue

was discussed

with TVA

materials

personnel

and the inspectors

determined that the materials

records

indicated that

650 pieces of WCSF-070-N of lot no.

15057

was received with

approximately

150 pieces

being issued to the plant.

The remainder of the

inventory was returned to Raychem.

The inspectors

examined

the warehouse

gA hold area,

main warehouse,

and the

auxiliary in plant warehouse

and

no inventory of WCSF-070-N of lot no.

15057

was found.

Several

installed .splices

were examined

in Unit 3 electrical

penetration junction boxes for penetrations

BA,

EC,

ED,

and in junction boxes

JB0107A and JB0107F

and

no splices utilizing WCSF-070-N of lot no.

15057 were

identified.

The inspectors

determined that the licensee's

corrective actions for LER 94-02

were adequate,

the item is closed.

5. 12

(CLOSED) IFI 50-296/95-37-01,

Verification of Emergency Lighting Levels

During

a

NRC inspection

(IR 50-296/95-37)

conducted

on July 17-21,

1995,

the

inspectors

observed

the location of the battery pack emergency lighting units

in the control

room and the operator

access

pathway to the backup

shutdown

panel

room.

The inspectors

also conducted

a "lights out

" test in the backup

shutdown

panel

room (electrical

board

room 3A) and the adjacent

480

V switch

gear

room.

This IFI was opened to track questions

raised

regarding

the location of other

emergency lighting fixtures needed for additional

manual

operations of safe

shutdown

systems

and access

and egress

routes to those plant locations

identified in the drafted post-fire Safe

Shutdown Instructions

(SSIs).

During this inspection

the inspector selected

a sample of Unit 3 rooms

and

plant pathways identified in the draft of 2/3-SSI-16,

Attachments

5 and 6, to

evaluate

the lighting installation

and arrangement

of the emergency lighting

system.

The inspector walked down the emergency lighting for operator

manual

actions

taken at the

480V

RMOV Boards,

250V

RMOV Boards,

and

4KV Shutdown

Boards.

During the walk down, the inspector verified by observation that the

arrangement

of the emergency lighting units were adequate

for operator

access

path illumination and board/panel

nameplate

illumination.

The inspector also reviewed the results of Post Modification Test

PMT-150,

Testing of Emergency Lighting System.

The

PMT inspection

was performed

on

August 28,

1995, to verify the functional status of Appendix

R lighting units

installed in the Unit 3 Reactor Building under

DCN W18755A to support Appendix

R safe

shutdown operator

manual

actions.

The test consisted of interruption

4.'Qi

i/i

33

of normal lighting, verifying and documenting illumination levels,

conducting

battery discharge tests,

and validation of the aiming of emergency lighting

heads.

Only'ne significant test deficiency was identified for a burned out

lamp on light number

143.

Work request

WR C307064

was

implemented to replace

the lamp and

was closed

on August 25,

1995.

Retest of the lighting unit was

performed with acceptable

results.

The inspector walked down

12 lighting

units listed in PHT.-150

and identified no discrepancies.

Based

on the location

and number of lighting units observed,

the inspector

concluded that the lighting arrangement

and levels in support of Unit 3 SSI-16

operator

manual

actions

were according to Appendix

R requirements.

Based

on

this observation

and the "lights out" performance test discussed

in IR 95-37,

Inspector

Follow-up Item 50-296/95-37-01

i's closed.

6.0

Exit Interview (30703)

'he

inspection

scope

and findings were

summarized

on October

18,

1995, with

those

persons

indicated in paragraph

1 above.

The inspectors

described

the

areas

inspected

and discussed

in detail the inspection findings listed below.

Although proprietary material

was reviewed during the inspection,

proprietary

information is not contained

in this report.

Dissenting

comments

were not

received

from the licensee.

Item Number

Status

Descri tion and Reference

GL 88-14

Closed

Instrument Air Supply Problems

Affecting Safety-Related

Equipment-

Unit 3 (paragraph

5. 1)

THI II.F.1.2.E

IFI 84-32-02

GS I 41/HPA B058

TI 2515/121

(GL 89-16)

LER'0-259,260,296/91-15

Closed

Closed

Closed

Closed

Closed

Suppression

Pool/Containment

Water

Level Monitor Unit 3 (paragraph

5.2)

Torus Narrow Range .Level

Instrumentation -Unit 3 (paragraph

5.3)

BWR Scram Discharge

Volume - Unit 3

(paragraph

5.4)

Verification of Mark I Hardened

Vent

Modifications

Unit 3 (paragraph

5.5)

HPCI

Low Suction Pressure - Unit 3

(Paragraph

5.6)

THI Action Item II.K.3. 28

.

Closed

gualification of ADS Accumulators .-

Unit 3 (paragraph

5.7)

~ ~

i

~gl

Igl

TMI II.K.3.13.B

LER 50-259,260,296/94-02

Closed

Closed

Separation

of High Pressure

Coolant

Injection and Reactor

Core Isolation

Cooling System Initiation Levels

Analysis

and Implementation

Unit 3

(paragraph

5.8)

Raychem Tubing for

EQ Applications,

(Paragraph

5. 11)

IFI 50-296/95-37-01

IFI 50-260/95-56-02

IFI 50-260/95-41-01

VIO 260,296/95-31-01

VIO 50-296/95-56-01

Closed

Open

Open

Open

Open

Verification of Emergency Lighting

Levels (paragraph

5. 12)

Use of Nickel-Based

Thread

Lubricants

on Gaskets

in TVA Class

"B" Fluid Systems

(paragraph

3.2)

EDG

1A Turbocharger

Inspection,

(paragraph

5.9)

Core Spray Testable

Check Valve

Testing not in Accordance with

Requirements,

(paragraph

5. 10)

Failure to Follow Alarm Response

Procedures

Results .in Loss of 480V

Bus (paragraph

2.3)

7,0

Acronyms

and Initialisms

ADS

AOI

ASME

ASOS

AUO

BFN

BWR

CAD

CAQR

CATD

CCD

CFR

CR

CRD

CS

DCA

DCN

DPR

EDG

EECW

EMD

EOI

Automatic Depressurization

System

Abnormal Operating Instruction

American Society of Mechanical

Engineers

Assistant Shift Operations

Supervisor

Auxiliary Unit Operators

Browns Ferry Nuclear Plant

Boiling Water Reactor

Containment

Atmosphere Dilution

Condition Adverse to Quality Report

Corrective Action Tracking Document

Configuration Control Drawing

Code of Federal

Regulations

Control

Room

Control

Rod Drive

Core Spray

Drawing Change Authorization

Design

Change Notice

Demonstration

Power Reactor

Emergency

Diesel

Generator

Emergency

Equipment Cooling Water

Electromotive Division

Emergency Operating Instructions

~ ~

A

~ .

4i

ig>

i/i

35

EQ

EQDP

ESF

FHE

GDC

GE

GL

GSI

HCU

HPCI

IFI

IR

IST

kv

LER

LOCA

MOV

NPA

MSIV

NCO

NPP

NR

NRR

NRC

OI

ORRT

PER

PHT

PORC

QA

QC

RCIC

RHR

RHRSW

RMOV

RPS

RWCU

SDIV

SDV

SER

SI

SIL

SPAE

SPOC

SRO

SSI

SSP

TDCN

TI

THI

TOE

TROI

Environmental Qualification

Environmental Qualification Documentation

Packages

Engineered

Safety Feature

Foreign Material Exclusion

General

Design Criteria

General Electric

P

Generic Letter

Generic Safety

Issue

,Hydraulic Control Unit

High Pressure

Coolant Injection

Inspector

Follow-up Item

Inspection

Report

Inservice testing

Kilovolts

Licensee

Event Report

Loss of Coolant Accident

Motor Operated

Valve

Multi-Plant Action Item

Hain, Steam Isolation Valve

Nuclear Commitment

Open

Item

Nuclear Performance

Plan

Narrow Range

Nuclear Reactor Regulation

Nuclear Regulatory

Commission

Operating Instruction

Operational

Readiness

Review Team

Problem Evaluation Report

Post Haintenance/Hodification

Test

Plant -Operations

Review Committee

Quality Assurance

Quality Control

Reactor, Core Isolation Cooling

Residual

Heat

Removal

Residual

Heat

Removal

Service

Water System

Reactor Hotor Operated

Valve

Reactor Protectionn

System

Reactor

Water Cleanup

Scram Discharge

Instrument

Volume

Scram Discharge

Volume

Safety Evaluation Report

Surveillance Instruction

Service

Information Letter

System Plant Acceptance

Evaluation

System Preoperational

Checklist

Senior Reactor Operator

Safe

Shutdown Instructions

Site Standard

Practices

Test Design

Change Notice

Temporary Instruction

Three Mile Island

Technical Operability Evaluation

Tracking

and Reporting of Open

Items

~ ~

I

i/i

<gt

TS

TSC

TVA

USI

VIO

WO

WP

WR 36

Technical Specifications

Technical

Support Center

Tennessee

Valley Authority

Unresolved Safety

Issue

Violation

Work Order

Work Plan

Work Request

gpss