ML18033B718

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Insp Rept 50-260/91-202 on 910415-19.No Violations Noted. Major Areas Inspected:Operations & Operations Support Activities,Unit Separation Program & Field Implementation & Corrective Actions Re Restart Concerns
ML18033B718
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 05/28/1991
From: Imbro E, Koltay P, Norkin D
Office of Nuclear Reactor Regulation
To:
Shared Package
ML18033B719 List:
References
50-260-91-202, NUDOCS 9106050264
Download: ML18033B718 (30)


See also: IR 05000260/1991202

Text

U.S.

NUCLEAR REGULATORY COMYiISSION

OFFICE

OF NUCLEAR REACTOR REGULATION

Division of Reactor Inspection

and Safeguards

NRC Inspection

Report:

50-260/91-202

License

No: DPR-52

Docket Nos:

50-260

Licensee:

Tennessee

Valley Authority

6N38 A Lookout Place

Chattanooga,

TN

37402-2801

Facility Name:

Browns Ferry Nuclear Plant Unit 2

Inspection

Conducted:

April 15-19,

1991

Inspection

Team:

NRC Consultants:

Peter S.,Koltay,

Team Leader,

NRR

John

V. Kauffman,

AEOD

Wayland

R. Bennett,

Senior Resident

Inspector,

RIV

David C. Lew, Resident

Inspector,

RI

David E. kills, Senior Resident

Inspector, RIII

4

Daniel

C. Ford, Parameter,

Inc.

Rene Vogt-Lowell, Parameter,

Inc.

Prepared

by:

Reviewed by:

Approved by:

Peter

.

ay,

Team Leade

Team Inspection

Development Section

A

Special

Inspection

Branch

Division of Reactor Inspection

and Safeguards

fice of Nuclear Reactor Regulation

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Team Inspection

Development Section

A

Special

Inspection

Branch

Division of Reactor Inspection

and Safeguards

Office of Nuclear Reactor Regulation

ugene

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m ro,

>>e

Special

Inspection

Branch

Division of Reactor Inspection

and Safeguards

Office of Nuclear Reactor Regulation

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4

EXECUTIVE SUMMARY

The

NRC operational

readiness

assessment

team

(ORAT) conducted

a followup

inspection at Browns Ferry Nuclear Power Plant from April 15 through April 19,

1991.

The objective was to continue to independently

assess

the Tennessee

Valley Authority's (TVA's) operational

readiness

to safely restart

and operate

the Browns Ferry Nuclear Plant, Unit 2.

The team focused its efforts in three

areas:

1.

Operations

and operations

support activities;

2.

The unit separation

program

and its field implementation;

3.

TVA's corrective actions in response

to restart

concerns identified during

the

ORAT inspection.

In the area of operations

and operation support,

the team's

assessment

remained

positive.

Licensee

personnel

performed activities both inside the control

room

and in the field professionally

and conservatively.

Operators

demonstrated

good

use of system operating

procedures,

except for several

minor deficiencies

which

were attributed to lack of attention to detail.

Examples

were failure to

initial to confirm completed steps,

and failure to observe

a radiation control

sign.

Continued

management

attention in this area is required in order to

reduce

the

number of those minor errors.

In one instance,

the shift supervisor failed to adequately

assess

plant condit-

ions prior to authorizing

a surveillance which, if carried out, would have

inadvertently

caused

a technical specification requirement to be violated.

Open

Item 50-260/91-202-01

concerns

the licensee's

corrective actions to (I) discuss

with shift supervision

the importance of properly assessing

plant status prior

to authorizing surveillances

and (2) revising the surveillance

procedure.

The Browns Ferry Unit 2 separation

program represented

a significant effort on

the part of the licensee

regarding

design reviews,

drawings identifying unit

separation,

system

and component labeling,

and installation of temporary bar-

riers.

At the time of the inspection,

corisiderable effort remained

in order to

assure

that this program would be thoroughly and effectively implemented.

Approximately 300 Unit 3 control devices

remained to be labeled.

The licensee

committed to complete the labeling of the control devices prior to Unit 2

restart after the team determined that the unit separation

program did not

include requirements for labeling of control devices

which actuate

Units I and

3

equipment required for Unit 2 operation.

Additionally, only 125 of 590 drawings

required for the program

had been

issued

and only 20 of these

had been partially

field verified by engineering

personnel.

"Significant work remained with regard

to the drawings, control device labeling,

and the training of plant personnel

on

program requireoients.

Subsequent

to the inspection,

the

NRC Resident

Inspector

verified the completion of this program.

Within the scope of its review, the team did not identify any issues that

would prevent it from recommending restart of Unit 2.

The team verified that

approprfate

corrective actions

were

implemented

by the licensee

to address

the

restart

concerns

which had been identified in the original

ORAT inspection.

However,

Open Item 260/91-201-03,

concerning

the fuel handling event,

remains

open pending

NRC review of the final incident investigation report.

TABLE OF CONTENTS

~Pa

e

1.0

INTRODUCTION ......................................................1

1.1

1.2

ackground ................................................

B

Inspection Objective and Scope ............................

~ ~ ~ 1

~ ~ ~ 1

.0

OPERATIONS ........................................................1

2

2.1

2.2

2.3

2.4

2.5

Obser vation of Control

Room Activities and Watchstanding

P ractices .................................................

Observation of Field Activities ...........................

Observation of Surveillance

and Maintenance Activities ....

System Walkdowns ........................;.................

Concluslons

~ ~ ~ o ~ s ~ ooo ~ ~ o ~ ~ o ~ oo ~ ~ ~ oo ~ ~

~ ~ ~ ~ ooo

~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ o ~

~ ~ ~ 1

~ ~ ~ 2

~ ~ ~ 3

~ ~ ~ 4

~ ~ 04

3.0

UNIT SEPARATION

PROGRAM

~ ~ o4

3.1

3.2

3.3

3.4

Review of System Drawings .................................

I.I~

System halkdowns ..........................................

Review of Training and Plant Personnel ....................

nt r

4

Conclusion

4

~ ~ ~ 5

~

~ ~ 6

~ ~ ~ 7

~ ~ ~ 7

t

4.0

FOLLOWUP ON RESTART

ISSUES

4.1

Determination of Responsibility for Communications

Between

Unit 2 and Unit 3 (Open Item 50-260/91-201-01) ............

4.2

Plant Operations

Review Committee

(PORC) Membership

(Open Item 50-260/91-201-02)

4.3

Power Ascension Test Program Procedures

(Open Item

50-260/91-201-06

and 50-260/91-201-07) ....................

4.4

Unit 1 Components

Required to be Functional

(Open Item

50 260/91

206 08)

~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~

~ ~ ~ ~ ~ ~ ~ ~ ~ ~

~ ~ ~ ~ ~ ~ ~

4.5

Rosemount Transmitter

Covers

(Open Item 50-260/91-201-11)

.

4.6

Incident Investigation Reports

(Open

Items 50-260/91-201-03

and 50-260/91-201-04) ..................,..................

~ ~ o7

~ ~ ~ 7

~ ~

~ 8

~ ~ ~ 8

~ ~ ~ 9

~ ~ ~ 9

~ ~

~ 9

4.6.1

Paint

Removal ............

4.6.2

Followup of Fuel Movement

Report (IIR)..............

~

~

~ ~ ~ ~ ~ ~ ~ ~ ~

~

~

~ ~ ~ ~ ~ ~ ~ ~

~

~ ~ ~ ~

Incident Investigation

~ ~

~ 9

~ ~ ~ 9

4.7

CGnclus 1 ons

~

~

~

~ ~ ~ ~

~ s

~ ~ ~ ~

~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ i ~ ~ ~ ~ ~ ~

~

~

~

~ ~ ~ ~ ~ ~ ~ ~ ~

~ ~ ~ ~ ~ ~ oil

5.0

EXIT MEETING .........................

~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~

~

~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ 11

APPENDIX A - Personnel

Attending Exit Meeti

9

o ~ ~ ~ ~

~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ oA

1

n

0

0

1.0

INTRODUCTION

1.1

Background

The

NRC operational

readiness

assessment

team

(ORAT) completed

a 2 week inspec-

tion effort at the Browns Ferry Nuclear

Power Station

on March 1, 1991.

The

results of the inspection

were detailed in NRC Inspection Report

No.

50-260/91-201

dated April 12, 1991.

The report

and

a letter to the licensee

dated

March 15, 1991, identified concerns

requiring corrective actions before

the restart of Unit 2.

Due to the plant status

during the previous inspection,

the team

recommended

a return visit to observe additional activities in an operational

environment.

The few activities that were evaluated

during the previous inspection,

specifically refueling and paint removal, did not in all cases

demonstrate

to

the team that all licensee activities would be conducted

in a conservative

manner.

Therefore,

NRC management

directed the team to return before restart

to continue its assessment

of Tennessee

Valley Authority (TVA) management's

control over the conduct of activities that affect plant operations.

The team

conducted its followup inspection from April 15 through April 19,

1991.

1.2

Inspection Objective and Scope

During the followup inspection the

team continue) with its independent

assess-

ment of TVA's operational

readiness

to restart Unit 2.

The team's efforts

focused

on three areas:

observation of activities affecting operations,

inside and outside the

control room, including watchstanding

and the conduct of maintenance

and

surv ei 1 lance

an in-depth assessment

of the unit separation

program including program

adequacy

and implementation

an evaluation of TVA's corrective actions in response

to concerns

identi-

fied by the

ORAT that required resolution before Unit 2 restart

2.0

OPERATIONS

During this inspection,

the team assessed

the implementation of the licensee's

requirements

and procedures for the conduct of operations

during

a 72-hour

continuous evaluation of shift activities in the control

room and throughout the

plant.

The team evaluated

operating philosophy, shift staffing,

and observed

shift turnover, shift operations, shift communications,

control

room access

and

personnel

conduct

and practices

associated

with operator plant tours

and

inspections.

2. 1

Observation of Control

Room Activities and Matchstanding Practices

The operating

crews demonstrated

a high level of professionalism,

enthusiasm,

and confidence

and were eager to return to power operations.

Shift personnel

strictly controlled access

to the control

room operating

area to exclude

workers not directly involved in ongoing or planned activities.

For example,

in one instance

a cleaning

crew was asked to leave the control

room horseshoe

area

so that it would not distract

a unit operator

responding

to a half scram.

0

II

Operator

response

to alarms

was timely and in accordance

with procedures,

and

communication to supervisors

was clear,

prompt,

and well understood.

Operator

knowledge of plant status

and reasons for alarms

was good.

The interaction

between control

room operators

and field personnel

during the performance of

surveillance

and maintenance activities was good.

Personnel

performed

normal

activities

such

as removal of a main turbine turning gear oil pump and bypassing

of a reactor water cleanup demineralizer in accordance

with the applicable

procedures.

All shift turnovers

observed

by the team during the 72-hour continuous

evalua-

tion of shift activities were detailed

and comprehensive.

Turnover briefings

were well conducted

and were attended

by plant operations

support personnel.

The shift staffing requirements

in the technical specifications

were met during

the observed shifts.

Logs were well written and

had the proper amount of

detail.

All required readings

were properly taken

and all required reviews

were performed

and documented

on the appropriate

logs.

The limiting conditions

for operations

(LCO) tracking program was properly implemented

during the

removal from service of the Unit 2 secondary

containment

and standby

gas treat-

ment systems.

The licensee

also effectively implemented activities outside the control

room

that could affect plant operations,

such

as the ongoing system draining and

realignment that were necessary

as

a result of the recently completed reactor

pressure

vessel

hydrostatic test.

These realignment activities were conducted

in accordance

with Procedure 2-SI-3.3.1.B,

"ASME Section

XI Hydrostatic Pressure

Testing of the Reactor

Pressure

Vessel

and Hain Steam Piping," and constituted

a

major portion of the activities during the period of this inspection.

The team observed

control room personnel

response

to two consecutive half scrams

caused

by

a spiking intermediate

range monitor

( IRH) in the neutron monitoring

system.

The licensee

had experienced

previous

problems with the neutron moni-

toring system

and was taking steps

to determine

the

cause

and to address

the

spiking problem.

This particular

IRM could not be bypassed

at the time of the

half scrams

because

another

IRH in the

same reactor protection

system

channel

was already

bypassed.

The team noted that the unit operator

used the applicable

annunciator

response

procedures,

verified that all required

alarms

had been

received,

and promptly contacted onshift instrument technicians

who responded

to

the control room.

The operator also sent

an auxiliary unit operator

(AUO) to

check for plant activities in the area of the

IRN preamplifiers that might

affect the instruments.

The team observed

good interactions

between

the shift

operations

supervisor,

his assistant

and the operations

superintendent.

2.2

Observation of Field Activities

The team observed

AUO rounds

and completion of corresponding

logs.

The

AUOs

were knowledgeable of the equipment

and demonstrated

good watchstanding

prac-

tices.

Cooeunication

between

AUOs and control

room personnel

was clear.

The

AUOs attended

turnover briefings and were knowledgeable of plant status.

Morale

appeared

to be good

among the AUOs.

Valve lineups after the hydrostatic testing

were completed in accordance

with

the hydrostatic testing procedure.

Good communications

between

the

AUOs in the

field and control

room personnel

were noted

by the team.

Removal,

accounta-

bilityy

and independent verification of configuration control tags were in

~

~

~

~

accordance

with plant procedures.

Coordination with health physics

personnel

with respect to the observed activities was adequate.

During the observation of shift activities, the team noted minor inconsisten-

cies in the implementation of procedural

requirements

and management

expectations.

During the performance of his rounds,

the

AUO did not have in his posses-

sion the

key required to open

an Emergency

Operating Instructions locker

located adjacent to the hydraulic control units.

The operations

superin-

tendent

informed the team that the

AUO should

have

had the

key in his

possession

during his rounds

and that this policy would be reiterated

during subsequent shift turnover meetings.

A number of items

( ladders,

welding rigs,

empty standby liquid control

barrels,

compressed

gas bottle carts,

MOVATS testing cart, etc.) found in

the reactor building lacked the required "llaterial In Use" tags.

The team

pointed these

out to the AUO.

A door with a "High Radiation - Door Must Be Locked

When Unattended"

sign

leading into the outboard

main steam isolation valve area

was open,

and

the area

was unattended.

The team verified that,

based

on the current

plant conditions,

a high radiation area did not exist within the subject

space.

However, the posted

requirements

fok this door were apparently

ignored rather

than modified to reflect actual radiological conditions.

2.3

Observation of Surveillance

and tlaintenance Activities

The team observed

several

maintenance

work planning

and status

meetings.

These,

meetings

were well conducted

and they ensured

scheduling,

communication,

and

allocation of resources

between various plant departments.

The team also

observed

and reviewed operations

surveillance

and post-maintenance

tests

and

determined that these activities were generally well conducted.

Personnel

were

knowledgeable

of independent verification program requirements

and independent

verifications were performed

as required.

During the residual

heat

removal service water

(RHRSW) initiation logic sur-

veillance

(Procedure

O-SI-428-67,

Revision 6) the team noted that the unit

operator

stopped

the surveillance

when

he realized that further conduct of the

surveillance

would place the plant in a condition prohibited by the Technical

Specifications.

The operator's

recognition of this discrepant

condition

indicated

a good overall

knowledge of plant status

and requirements.

However,

shift supervision

had performed

an inadequate

review before authorizing the

performance of the surveillance

in that off-normal conditions

had not been

properly considered.

The procedure

directed the operator to place the emergency

equipment cooling water

(EECM)

pump

B3 control switch to the pull-to-lock posit-

ion, thus disabling

pump

B3 and leaving only

EECW pump

D3 to supply the south

EECh header.

Since the emergency

power supply for EECW pump

D3 was inoperable,

this

pump was also considered technically inoperable while the plant was in the

cold shutdown condition.

Technical Specification Table 3.5. 1 required at least

one operable

EECW pump per header.

I

fr

0

The team brought the inadequate

review by the shift supervision to the atten-

tion of the licensee.

The manager of operations

stated that the corrective

action would be two fold, (I) discuss with shift supervision

the importance of

properly assessing

plant status prior to authorizing surveillance activities,

and (2) correct the procedure to assure

that the requirements

of Technical

Specification Table 3.5.1 could not be inadvertently violated during the

surveillance.

The licensee's

corrective actions will be followed as

an open

item (Open Item '50-260/91-202-01).

The team observed additional maintenance

work and post-maintenance

testing to

determine if the activities were being properly conducted

in accordance

with

plant procedures.

Althou'gh these activities were generally well performed,

the

following minor problems

were noted in the work order documentation:

WO 91-28934-00

and

WO 91-24429-00

were modified to remove quality control

(gC) holdpoints.

However, the documentation

did not identify the

gC person

notified of the action,

as required

by Procedure

SDSP-7.6.2,

"Planning Work

Orders" (Revision 11).

A work planner forgot to provide this information to

the job foreman who, in turn, did not question its absence.

Completion of the pre-job briefing and personnel

safety analysis

was not

documented

in

WO 90-23937-00,

as required

by Procedure

SDSP-7.6.5

"Perfor-

mance of Work Orders,"

(Revision 11).

4

After the

team informed the licensee

about these

examples,

the licensee

com-

pleted the required documentation.

2.4

System

Walkdowns

The team performed walkdowns of the standby

gas treatment

system,

Unit 2 core

spray system,

the U>>it I

RHRSW system

and the Unit I residual

heat

removal

system to ascertain

system status

and coridition.

These

systems

appeared

to be

adequately

maintained,

selected

lineups were correct

and selected

clearances

were correctly placed.

The team noted that the locked valve program was

implemented.

Valves required to be locked were verified by the team to be in

the correct position.

2.5

Conclusions

Routine operations shift activities were conducted

in a professional

manner

inside

and outside the control room.

Shift personnel

demonstrated

good under-

standing

and use of procedures.

However, minor problems were indicative of lack

of attention to detail

in several

areas

such

as failure to initial procedure

steps, failure to observe

a radiatiori control sign,

and lack of material

controls in the reactor building.

In one instance,

the shift supervisor failed

to adequately

assess

plant conditions prior to authorizing

a surveillance

which,

if carried out, would have inadvertently

caused

a technical specification

requirement to be violated.

The discrepancies

were brought to the licensee's

attention,

and the licensee initiated prompt corrective actions.

3.0

UNIT SEPARATION

PROGRAM

To assure

operability of technical'specification

equipment

and operational

separation

of the Browns Ferry units, the licensee

has developed

and imple-

mented

a program of unit separation for recovery activities.

The program,

0

which was defined in Site Standard

Practice

SSP-12.50,

"Unit Separation for

Recovery Activities," established

control of personnel

access

and system

operational

interfaces.

The controls were designed

to restrict access

into

Unit 2 operating

areas

by Unit 3 recovery personnel

and to ensure that Unit 3

recovery

and Unit 1 layup activities did not affect Unit 2 systems.

The team's

review of this program included

an overview of personnel

training;

interviews with plant personnel;

an assessment

of the development,

approval,

distribution,

and verification of interface drawing;

and the walkdown of

several

plant systems

to assess

labeling of boundary

and unit interfaces

and

personnel

access

barriers.

The review of SSP-12.50

showed that the licensee's

program provided

a compre-

hensive

approach

to unit separation.

Particular

emphasis

was placed

on con-

trols that limited access

of nonessential

personnel

into Unit 2 operating

areas.

Special

provisions were

made for badging, training,

and qualification of

personnel

who would require access

to these

areas

during Unit 2 operation.

The

team considered restrictions established for personnel

access

to be adequate if

properly implemented.

The program also established

requirements for the

identification and control of system operational

interfaces.

3. 1

Review of System Drawings

To identify plant systems physically located in Units

1 and

3 and required to

support Unit 2 operation,

the licensee

issued

a Series of system drawings that

indicated unit boundaries for systems

shared

between units.

The drawings

did not represent

a change

in configuration of plant design, but applied

a

system of color coding to assist plant personnel

in identifying operational

interfaces

between units.

The team reviewed the licensee's

process for development,

approval

and distri-

bution of interface drawings.

The process

incorporated

input from system

engineers

and operational

personnel

in order to identify system boundaries

and

plant operational

interfaces.

Design reviews included

an assessment

of flow

diagrams,

schematics,

single line electrical drawings,

and electrical

power

supply requirements for plant interface systems.

Drawings annotated

to reflect

the above were then forwarded to nuclear

Engineering for review and approval

before the production of computer assisted

design

(CAD) enhancements.

Following

CAD development

the drawings received additional consistency

reviews before they

were distributed.

Once the drawings

have

been

issued,

engineering

personnel

verified by physical

walkdown that affected plant systems

and components

were

labeled in accordance

with drawing and procedural

requirements.

The licensee's

verification was being accomplished

in two phases.

Phase

One covered piping and

Phase

two covered

components.

At the time of the inspection,

20 drawings

had

been partially verified (Phase

One)

and

none

had been fully verified.

Additi-

onally, the plant design

change control program was modified to ensure that unit

separation

was considered for future plant modifications.

To determine

the effectiveness

of this program,

the team reviewed

17 drawings

that

had

been

issued

and partially verified by the licensee.

The review showed

that the licensee's

program for development,

approval

and distribution of these

drawings

was accomplished

in accordance

with program requirements.

The team

also noted that the drawings were sufficiently detailed

and clear to enable

plant personnel

to readily identify operational

interface points.

Although most

programmatic

aspects

of this process

were adequate,

of the approximately

590

0

4

I]

fi

e

drawings required for this effort, only 125 had been

issued at the time of this

inspection.

Of these,

only 20 had been partially field verified by engineering

personnel,

as indicated

above.

Subsequent

to the inspection,

the

HRC Resident

Inspector verified implementation of this program.

3.2

System Walkdowns

The team performed walkdowns of several

systems

using

17 system drawings

issued

and partially verified by the licensee.

The walkdowns focused

upon aspects

of

system

and component

labeling required

by the unit separation

program.

The team

compared

drawing requirements

with the labeling of piping, instrumentation,

electrical,

mechanical,

and support systems.

Labeling consisted

of orange

tape

that was applied to system piping and equipment,

and of Unit 2 operation caution

tags that were applied to electrical panels, circuit breakers

and various other

equipment.

In general,

the plant systems

were labeled

as required

by the

drawings.

The labels provided distinct identification of interfacing

compo-

nents.

However,

two valves in the generator

hydrogen

system

had interface

boundary labels which were not required

by applicable

system drawings.

Since

labeling for these

valves

was recorded

in the manual

log which was kept for all

labels installed in the field, the licensee's

verification program would have

reasonably

been

expected to identify this error.

The team examined portions of the

125

VDC system.

Drawings for this system

had

not been

issued formally, but were provided as "jnformation only" for the

purpose of this inspection.

In general,

the affected

components

were labeled

as required.

However, the control devices

which actuate

Unit 3 and Unit I

equipment required for Unit 2 operation

had not been

labeled to restrict their

use.

These devices

included

hand switches for the Unit 3 diesel

generator air

compressors

and diesel

room essential

exhaust fans,

and

a pushbutton

station'or

a Unit I standby

coolant system valve.

During subsequent

discussions

with

engineering

personnel,

the team found that the unit separation

program did not

include requirements for labeling control devices.

The team concluded that

this inconsistency

in labeling could lead to the improper manipulation of the

control devices

by plant personnel.

In response

to this concern,

the licensee

planned to enhance

the unit separa-

tion program by labeling Unit 3 control devices that might affect Unit 2

operation.

The approximately

300 devices

would be labeled before the restart of

Unit 2.

The

NRC Resident

Inspector

subsequently

verified implementation of

those actions.

Temporarily installed barriers,

designed

and fabricated for the unit separation

program, prohibited the entrance

of unauthorized

personnel

into Unit 2 operat-

ing areas.

The team expressed

a concern that these barriers

could preclude the

movement of auxiliary unit operators

(AUO) during

a response

to abnormal plant

operating conditions.

The licensee

stated that,

based

upon the r~view of plant

and emergency

operating

procedures,

no adverse

impact had been identified.

After further review, the team agreed with the licensee's

conclusion.

3.3

Review of Training and Plant Personnel

The team reviewed the licensee's

general

employee training

(GET) program with

respect

to unit separation.

Corporate

access

training was specified

by

GET

0

course

010, "Nuclear Industrial Training/Retraining."

This course is provided

annually to personnel

requiring access

to Browns Ferry and included

site-specific training for personnel

and

a

15 minute film on the unit separa-

tion program.

Basic aspects

of the program,

including the significance of

color coding, the identification of components affecting Unit 2 operation

and

area

access

controls,

were discussed

iri the film.

Currently,

more than

2300 employees

have viewed the film and approximately

300

personnel

remain to be trained.

Additionally, the licensee

planned to perform

formal classroom training, covering the details of the unit separation

program,

for all operations

personnel

prior to restart.

The classroom training would be

incorporated

into the operator's

requalification trairiing program.

Subsequent

to the inspection,

the

NRC Resident

Inspector verified implementation of this

program.

3.4

Conclusions

The Browns Ferry unit separation

program represented

a significant effort on

the part of the licensee

regarding

design reviews,

drawings identifying unit

separation,

system

and

component labeling,

and installation of temporary

access

barriers.

At the time of inspection,

considerable effort remained in order to

assure

that this program would be thoroughly and effectively implemented.

This

effort involved the labeling of Unit 3 control devices

required for Unit 2 oper-

ation, verification of separation

drawings,

arid detailed training of operations

personnel.

Subsequent

to the inspection,

the

NR0 Resident

Inspector verified

the completion of this program.

4.0

FOLLOWUP ON RESTART ISSUES

NRC inspection report 50-260/91-201 identified open

items that required resolu-

tion before Unit 2 restart.

During this irispection period, the licensee's

corrective actions in response

to the open

items were assessed

by the team.

4.1

Determination of Responsibility for Communicatioris

Between Unit 2

and Unit 3 (Operi Item 50-260/91-201-01)

The licensee

committed to establish

administrative controls delineating

respon-

sibilitiess

for communications

between

the Unit 2 and

3 site organizations

at

management

levels.

The licensee

has initiated the development of a formalized administrative

program to delineate responsibilities

and lines of communication

between

Browns

Ferry (BF) operations

and

BF restart organizations.

The licensee's

memorandum,

dated April 18,

1991 identified (1) the responsibilities of the

BF operations

and restart organizations

management,

(2)

BF operations

and restart organiza-

tions,

and (3) individual restart

issues

and detailed division of resporsibi li-

ties for each of these

issues.

The memorandum also specified the existing

BF hierarchy of site procedure

as it

was applicable to Unit 1 and Unit 3 recovery,

in coordination with the Unit 1

and Unit 3 Restart Project Procedures

Manual.

However, the memorandum

recog-

nized the

need for additional

procedures

in two areas:

(1)

a

new site standard

practice

(SSP 1.5) to clarify the role of the Unit 1 and Unit 3 restart organ-

izations

as part of the

BF site organization

and (2)

a dedicated

series of

procedures

would be issued to address

specific activities identified in the

Restart Project Procedures

Manual.

The licensee

stated that these

procedures

were under development

and would be issued

by June 1, 1991.

Based

on the licensee's

corrective actions,

which established

the administrative

controls delineating

the lines of communication

between

the Unit 2 and Unit 3

site organizations

and the licensee's

commitment to develop additional

procedures

as indicated above,

the team considers this item closed.

The actions

completed

satisfy the team's

concerns for restart.

4.2

Plant Operations

Review Committee

(PORC) Membership

(Open Item

50-260/91-201-02)

The team identified that Technical Specification Section 6.5.1.2 did not

correctly designate

committee

members

by their current titles.

On March 1, 1991, the licensee

submitted

a technical specification

change

which

revised the

PORC composition.

The revision accurately reflected existing

membership titles.

Additionally the licensee

also revised Site Director

Standard

Procedure

(SDSP) 27.4,

PORC, to incorporate title changes,

delineate

membership responsibilities,

and define

a methodology for designation of

alternate

committee memberships.

The team considers this item closed for the

purpose of this inspection.

Review and approval of the license

amendment will

be in accordance

with NRC procedures.

4.3

Power Ascension Test Program Procedures

(Open

Items 50-260/91-201-06

and

50-260/91-201-07)

Several

required items,

such

as functional organization, shift staffing, review

of procedural

references,

and independent

review of test results,

were not

included in applicable Plant Manager Instructions

(PMI) 26.1,

"Power Ascension

Test Program,"

and

PMI- 17.1,

"Conduct of Testing."

Additionally, technical

deficiencies

were identified in several test procedures

of the power ascension

test program.

The team verified that procedures

PMI 26.1

and

PMI 17.1

have

been revised to

incorporate

the above required

items.

The team also reviewed test procedures

and verified that actions

were being taken to correct the technical

deficiencies.

The team considers this item closed.

4.4

Units

1 and

3 Components

Required to be Functional

(Open Item

50-260/91-206-08)

The licensee

has identified the systems

and components

in Units

1 and

3 that

were required to be operable to support Unit 2 operations.

The licensee

indicated that certain

components

in Units

1 and

3 were required to be func-

tional to support the Units

1 and

3 systems

required to be operable.

The team

requested

that the licensee

identify the specific Unit 1 and

3 components

that

have to be functional

and define for these

components

.he requirements

that

have to be met to assure

they are functional.

During this inspection,

the licensee

stated

and the team verified, that the

above referenced

"functional" equipment, e.g.,

the Unit

1 torus which is

required to test the operability of Unit 1 residual

heat

removal

pumps,

continued to remain under the work control programs that were in place for

Unit 2 equipment.

The team considers

that this would ensure

the continued

operability of equipment required to support Units

1 and

3 systems

required to

be operable.

The team considers this item closed.

4.5

Rosemount Transmitter

Covers

(Open Item 50-260/91-201-11)

The team reviewed licensee

actions in response

to the concerns

about excessive

gaps discovered

between

nine Rosemount transmitter electronic side covers

and

housings.

A licensee

review indicated that only one of the transmitters,

2-PT-64-67,

was of concern.

The remainder either were not environmentally

qualified equipment,

and therefore

had

no specific cover torque requirements,

or had not yet been calibrated following installation.

Torque was purposely

not applied during installation because

removing the covers for subsequent

calibration adjustment

before startup would have necessitated

the replacement

of o-rings.

During its review of maintenance

history, the licensee

could not determine

a

root cause for the loose cover on drywell pressure

transmitter 2-PT-64-67.

Documentation

indicated that proper torque

was verified by a

gC holdpoint

during calibration in 1988.

Subsequent

calibration surveillance

did not

necessitate

the removal of the cover because

adjustments

were not necessary.

After the

NRC had identified the problem, the licensee

properly torqued the

transmitter

cover and provided training to instrument technicians

to emphasize

the importance of proper cover torque.

The team determined that the surveil-

lance procedure,

2-SI-4.2.F-3(B),

"Drywell Pressure

Channel Calibration"

(Revision 3), was adequate

in this regard since

a specific torque requirement

was prescribed if the cover was

removed.

The team considers this item closed.

4.6

Incident Investigation Reports

(Open Item 260/91-201-03

and 50-260/

91-201-04)

During the

ORAT inspection

the team noted that in two instances,

paint removal

and initial fuel movement,

the licensee failed to recognize

and assess

the

potential

impact of the activities

on plant safety.

The licensee

stated that

incident investigation reports would be prepared.

4.6.1

Paint

Removal

The team inspected

equipment potentially affected

by dust from the surface

preparations,

i.e., portions of the Unit 2 reactor building and internals of

motor control centers

(tlCCs).

No discrepancies

were identified and the

NCCs

were clean.

The team reviewed Final Event Report II-B-91-038, "Reactor Building Painting."

The report identified weaknesses

in the applicable

procedure,

t)AI-5.3,

Protective Coatings,

Revision 5, as the root cause for the event.

The

procedure

contained

requirements fur dust control, but did not specify

4

(j

~

~

~

~

~

~

~

lines of responsibility for implementing action

and verification of such

controls.

Subsequently,

the licensee

assigned

responsibility for the implemen-

tation of protective actions to the operation

department.

The team verified

that the lines of responsibility were detailed

in revision

6 of the above

procedure.

The team considers this item closed.

4.6.2

Followup of Fuel Novement Incident Investigation Report

( IIR)

The team reviewed Final Event Report II-B-91-040, "Source

Range Nonitor/Fuel

Load Chamber

Noise Spikes

Occurring

on 2/21/91."

The team noted that the

licensee

was apparently reluctant to expand the scope of the incident investi-

gation beyond the technical

issue of reactor protection

system operability and

justification of the acceptability of licensee

actions during the event.

Accordingly, the

team found that the IIR did not provide (I) a detailed

and

comprehensive

root cause analysis,

or (2) comprehensive

corrective actions to

prevent recurrence.

The team determined that potential failures to "B" SRN during planned fuel

movement were indicated to shift and management

personnel

by erratic

SRN

response

and failure to implement work request

requirements

(WO No. C042091)

for troubleshooting,

repair,

and post-maintenance

testing of the

SRN.

In view

of this situation,

the team concluded that the decision to initiate fuel

movement

was inappropriate

since this potentially inoperable

SRN would have

precluded

compliance with precautions

identified, in procedure

2-GOI-100-3,

"Refueling Operations,"

and requirements for two operable

SRNs

as stated

in

t

Technical Specification Section 3.10.B.1.

The team also noted the following discrepancies

in the data presented

in the

investigation report:

WO PC042091

was written before fuel movement to "troubleshoot

and rework

as required to restore

2-SRN-92-B and/or

FLC to perform as intended."

Subsequently,

the work request

was closed without completing specific

tasks.

The report failed to address

the basis for closing the work

request without completing the work.

The incident investigation report indicated that only "Hi" spikes

were

received

on "B" SRN before the initial fuel movement.

However, written

statements

from two licensed shift crew members

indicated that "Hi Hi"

spikes

were received at the

SRN local panel before

WO PC042091

was initi-

ated

and before initial fuel movement.

These

two crew members,

when

interviewed

by the

ORAT team, maintained that their written statements

were accurate.

However, the team determined that poor control

room log

keeping during this event apparently contributed to the loss of pertinent

information concerning

the above discrepancy,

such

as the type of alarms

received,

the sequence

of events,

the status of shorting links and the

position of the

SRN bypass

switch.

The licensee

acknowledged that the quality of incident investigation reports

needed

to be enhanced

through training of personnel.

In addition, the licensee

1

initiated

a

Human Performance

Enhancement

System

(HPES) evaluation of this

event

and planned to revise the final incident investigation report,

as approp-

riate,

bzsed

on the

HPES evaluatiox.

The team conducted

a preliminary review of

10

0

the

HPES findings and determined that the licensee's

corrective actions

appeared

~

~

~

~

~

~

~

~

to have adequately

addressed

the restart implications of these

issues.

This

item, while no longer

a startup

issue,

remains

open pending

NRC review of the

final incident investigation report.

4.7

Conclusions

The team verified that appropriate

corrective actions

were implemented

by the

licensee

to address

the restart

concerns.

However,

Open Item 260/91-201-03,

concerning

the fuel handling event,

remains

open pending

NRC review of the

final incident investigation report.

5.0

EXIT MEETING

On April 19,

1991, the team conducted

an exit meeting at the Drowns Ferry site.

Licensee

and

NRC representatives

attending this meeting

are listed in

Appendix A.

During the exit meeting,

the team summarized

the scope

and find-

ings of the inspection.

0

. APPENDIX A

Personnel

Attendin

Exit Heetin

NRC

Wayland

R. Bennett,

Senior Resident Inspector,

RIV

Edward F. Christnot, Resident

Inspector,

Browns Ferry

Stewart

D. Ebneter,

Regional Administrator, RII

Daniel

C. Ford, Parameter,

Inc.

Brian K. Grimes, Director, Division of Reactor Inspection

and Safeguards,

NRR

Frederick J.

Hebdon, Project Director, Project Directorate II-4, NRR

David E. Hills, Senior Resident

Inspector,

Region III

Gary H. Holahan,

Deputy Director, Division of System Technology,

NRR

John

V. Kauffman,

AEOD

Paul J. Kellogg, Section Chief, RII

David C.

Lew, Resident

Inspector,

RI

Rene Vogt-Lowell, Parameter,

Inc.

Dr. Thomas

E. Hurley, Director,

NRR

Donald P. Norkin, Section Chief, SIB, DRIS,

NRR

James

G. Partlow, Associate Director for Projects,

NRR

Thierry H. Ross, Project Hanager,

NRR

Tennessee

Valle

Authorit

t

Hasoud Bajestani,

Technical Support Manager

Paul

R. Baron, Quality Control Hanager

Joe

Bynum, Vice President,

Nuclear Operations

Patrick P. Carier, Site Licensing Hanager

Hax E. Herrell, Plant Operations

Hanager

Hark 0. Hedford, Vice President,

Nuclear Assurance,

Licensing

and Fuels

Dan A. Nauman, Senior Vice President,

Nuclear

Power

John L. Sparks,

Technical

Support

Gerald

G. Turner, Site Quality Hanager

Oswald J. Zerigue, Site Director

F

4