ML16341E948

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Insp Repts 50-275/88-31 & 50-323/88-29 on 881023-1203. Violations Noted.Major Areas Inspected:Plant Operations, Maint & Surveillance Activities,Followup of Onsite Events, Open Items,Lers & Selected Independent Insp Activities
ML16341E948
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 12/20/1988
From: Johnston K, Mendonca M, Narbut P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML16341E947 List:
References
50-275-88-31, 50-323-88-29, NUDOCS 8901170263
Download: ML16341E948 (58)


See also: IR 05000275/1988031

Text

U.

S.

NUCLEAR REGULATORY COMMISSION

REGION V

Report Nos:

50-275/88-31

and 50-323/88-29

Docket Nos:

50-275

and 50-323

License

Nos:

DPR-80 and DPR-82

Licensee:

Pacific Gas

and Electric Company

77 Beale, Street,

Room 1451

San Francisco,

California 94106

Facility Name:

Inspection at:

Diablo Canyon Units 1 and 2

Diablo Canyon Site,

San Luis Obispo County, California

Inspection

Conducted:

October

23 through

December 3,

1988

K.

E. Johnston,

Resident Inspector

P.

P.

Narbut, Senior Resident

Inspec or

~Z~e

Approved by:

Y>C

>opfI'ate

Signed

g z. Q~~/I'V

Date Signed

M.

M. Mendonca,

Chief, Reactor Projects

Section

1

Date Signed

Summary:

Ins ection from October

23 throu

h December

3

1988

Re ort Nos.

50-275/88"31

~/

Areas Ins ected:

The inspection

included routine inspections of plant

operations,

maintenance

and surveillance activities, follow-up of onsite

events,

open items,

and licensee

event reports

(LERs),

as well as selected

independent

inspection activities.

Inspection

Procedures

30703,

36700,

61726,

62700,

62703,

71707,

92700,

92701,

92720,

93702,

and 94703 were used

as

guidance during this inspection.

Results of Ins ection:

One violation was identified regarding the failure of

a test engineer to follow a procedure

as described in paragraph 6.a..

No

deviations

were identified.

Areas of Stren ths

o

Although it occurred

immediately after the reporting period (on December

5, 1988) the licensee

notably achieved

a "black board"

on Unit 1.

This

effort reduced

the number of lit annunciators

during normal operation

from approximately

40 (two years

ago) to zero.

89011 70263 881220

PDR

ADOCK OSDO0275

G

PNU

o

The licensee's

management

response

to the

damage

and loss of a Unit 2

residual

heat

removal

pump while in a midloop condition was considered

to

be timely, thorough,

and commendably conservative.

The action plan

generated

and executed

was detailed

and actions specified were carried

out in formal ways such

as the issuance

of a temporary operating

procedure.

Areas of Weakness

Instances

of valve lineup problems

were emphasized

in the last resident

inspector

report (50-275/88-26).

Additional examples of valve lineup

problems occurred during this reporting period which reemphasize

the

need

for licensee

action.

Specifically, this report discusses

the discovery

of missing position seals

on an auxiliary feedwater

pump recirculation

valve (paragraph 3.b.), the-discovery of a mispositioned valve providing

sample air to the containment

vent noble gas radiation monitor (paragraph

4'.) and the unplanned

closure of the suction valve to a running safety

injection pump (paragraph

4. i. ).

Associated with the valve lineup

problems,

paragraph

11.b.

discusses

several

instances

of ineffective

action

on the part of quality surveillance

personnel

conducting valve

lineup survei llances.

This report contains

several

examples

of operator error and/or lack of

operator attention,

which, coupled with the inattentive overfilling of a

steam generator

discussed

in the last resident inspector report

(50-275/88-26)

indicates

the

need for management

attention.

This report

discusses

a lack of operator attention in removing

a clearance

which led

to the

damage of running safety injection pump (paragraph 4.i.),

a lack

of operator attention resulting in four actuations

of the low temperature

overpressure

protection devices

(paragraph 4.o.),

and operator error in

failing to recognize

a need to perform compensatory

action when a

quadrant

power tilt ratio alarm was generated

dur ing nuclear instrument

calibrations

(paragraph

4. h. ).

o

The violation, identified in this report regarding

a test engineer

not

following procedure

for reading

an erratic

gauge during a surveillance

test, is a particularly noteworthy since the licensee

has

been

ineffective in resolving the previously identified problem of adequately

reading test instrumentation.

A similar violation was identified earlier

in February

1988.

Subsequently,

in September

1988,

a notice of deviation

was issued

because

the licensee

had not issued

a procedure

as committed

in the violation response.

The procedure

was subsequently

issued but

personnel

were apparently

not informed or trained in its use.

The issue

of ineffective communication of expectations

was also

a concern of the

most recent

SALP report and this violation reenforces

the

need for

continued

management

action.

DETAILS

1.

Persons

Contacted

"J.

D.

Townsend,

Plant Manager

"D.

B. Miklush, Assistant Plant Manager,

Maintenance

Services

"L. F.

Womack, Assistant Plant Manager,

Operations

Services

"B.

W. Giffin, Assistant Plant Manager,

Technical

Services

J.

M. Gisclon, Assistant Plant Manager for Support Services

C.

L. Eldridge, guality Control Manager

K.

C.

Doss,

Onsite Safety

Review Group

T.

A. Bennett,

Maintenance

Manager

W.

G. Crockett,

Instrumentation

and Control Maintenance

Manager

J.

V. Boots,

Chemistry

and Radiation Protection

Manager

T.

L. Grebel,

Regulatory

Compliance Supervisor

S. R.'ridley, Operations

Manager

R.

P.

Powers,

Radiation Protection

Manager

  • W. J. Kelly, Compliance

Engineer

"S.

M. Skidmore, guality Assurance

Manager

"D. A. Taggert, guality Surveillance Supervisor

"W. T.

Rapp,

Onsite

Review Group. Chairman

  • W.

D. Barkhuff, Senior guality Control Engineer

  • T. J. Martin, Training Manager

The inspectors

interviewed several

other licensee

employees

including

shift foremen

(SFM), reactor

and auxiliary operators,

maintenance

personnel,

plant technicians

and engineers,

quality assurance

personnel

and general

construction/startup

personnel.

  • Denotes those attending the exit interview on December

12,

1988.

0 erational

Status of Diablo Can

on Units 1 and

2

Unit 1 was in power operations

at the beginning of the reporting period

and remained

so during the reporting period.

No reactor trips or

significant events

occurred.

Reportable

events

such

as containment

ventilation isolation occurred

as detailed in Section

4 of this report.

Unit 2 remained

in its second refueling outage for the reporting period.

The period began with fuel load just completed

and ended with the unit in

Mode 3 in preparation for return to service.

During the period numerous

events

occurred

as detailed in Section

4 of this report.

The most

notable of these

events

included severe

damage to two safety related

pumps; specifically,

a residual

heat removal

pump was

damaged

due to an

reassembly

error and

a safety injection pump was

damaged

due to operator

error in .processing

a clearance.

~ ~

3 .

0 erational

Safet

Ver ification

7l707

a.

Gener al

During the inspection period, the inspectors

observed

and examined

activities to verify the operational

safety of the licensee's

facility.

The observations

and examinations of those activities

were conducted

on a daily, weekly or monthly basis.

On a daily basis,

the inspectors

observed control

room activities to

verify compliance with selected

Limiting Conditions for Operations

(LCOs) as prescribed in the facility Technical Specifications

(TS).

Logs, instrumentation,

recorder traces,

and other operational

records

were examined to obtain information on plant conditions,

and

trends

were reviewed for compliance with regulatory requirements.

Shift turnovers

were observed

on a sample basis to verify that all

pertinent information of plant status

was relayed.

During each

week, the inspectors

toured the accessible

areas of the facility to

observe

the following:.

(a)

General

plant and equipment conditions.

(b)

Fire hazards

and fire fighting equipment.

(c)

Radiation protection controls.

(d)

Conduct of selected activities for compliance with the

licensee's

administrative controls

and approved procedures.

(e)

Interiors of electrical

and control panels.

(f)

Implementation of selected portions of the licensee's

physical

security plan.

(g)

Plant housekeeping

and cleanliness.

(h)

Engineered

safety feature

equipment alignment

and conditions.

(i)

Storage of pressurized

gas bottles.

The inspectors

talked with operators

in the control room,

and other

plant personnel.

The discussions

centered

on pertinent topics of

general

plant conditions,

procedures,

security, training,

and other

aspects

of the involved work activities.

b.

Auxiliar

Feedwater

Pum

Recirculation Sto

Valve Missin

Seal

On November 9, 1988, during a routine walkdown of the Unit 1

auxiliary building, the inspector discovered

valve FW"1"189, the

auxiliary feedwater

(AFW) motor driven pump 1-3 recirculation stop

valve,

was not sealed.

The inspector brought this to the attention

of the Shift Foreman.

A subsequent

review by the inspector of the applicable

sealed

valve

check list for the

AFW system revealed that the valve was required

to be sealed

in the'throttled position.

The monthly pump test

requires that the valve be throttled to allow between

49 and 51

gpm

recirculation flow with discharge

to the steam generator

isolated.

The inspector discussed

these findings with the shift supervisor

who

concluded that to determine if the valve was in the appropriate

position

an "as found" position was to be determined

(one quart'er

turn open),

and

a partial

pump test to be performed.

Initially,

during the

pump test,

the recirculation flow gage

read

between

40

and 140 inches of water, well outside the acceptance

criteria of 96

to 104 inches of water which corresponds

to between

49 and 51 gpm.

However,

due to erratic readings,

the gauge

was suspected

of being

inaccurate.

The gage

was

removed

and a new gauge

was installed.

The second

reading determined that recirculation flow was

50 gpm and

that the valve's

as found position was appropriate.

The inspector

discussed

this repeat

occurrence of a valve missing

its seal

(see inspection report 50-275/88-26) with the Operations

'Manager.

In the last inspection report, the Operations

Manager

described

a

new procedure for sealed

valves.

As a result of this

finding and others

by operations,

the licensee

is continuing to

review the sealed

valve program for adequacy

and

has initiated

a

equality Evaluation.

In addition,

an Action Request

was initiated to

evaluate

the

bad gauge.

The inspectors will continue to follow-up

the licensee's

corrective actions with regards, to the sealed

valve

program.

No violations or deviations

were identified.

4.

Onsite

Event Follow-u

93702

Unit 1 Inadvertent

Containment Ventilation Isolation

On November 2, 1988,

an auxiliary operator

erroneously

source

check

tested

the wrong monitor in the process

of source

check testing the

liquid radwaste radiation monitor RM-18,

a prerequisite for a liquid

r adwaste

discharge.

The, operator tes'ted the plant vent gas

radiation monitor (RM-148), causing

a containment ventilation

isolation (CVI).

The event was reported

as

a four hour

non-emergency

event and was also 'the subject of LER 1-88-23.

The

erroneous

source

check of RM-148 and consequent

CVI happened twice

in 1987.

Corrective actions taken in 1987 included implementation

of a source

check procedure

and improved labelling (red labels

on

all radiation monitors whose actuation results in a CVI).

Corrective

action for this most recent events

includes the

installation of plexiglass

covers

on radiation monitors which can

cause

a CVI.

The licensee

considers that the installation of covers

will inhibit operators

from source

checking the wrong radiation

monitor.

0

b.

Unit 2 Residual

Heat

Removal

Pum

2-2 Failure

On November

3, 1988, the lower motor bearing for Residual

Heat

Removal

(RHR) pump 2-2 failed shortly following its start.

It was

discovered

by an auxiliary operator

who smelled

and subsequently

saw

smoke

coming from the pump.

The pump was immediately shut

down

from the control

room.

The unit was in Mode

5 with the reactor coolant loops partially

filled.

This condition required both

RHR pumps to be operable

since

the

RHR pumps were the only normal

and available

way to remove core

decay heat.

With the reactor coolant loops not filled, the steam

generators

were not available

as

a heat

removal

mechanism.

Other plant conditions

germane to the event were that the

containment

equipment hatch

was

open (containment integrity is not

required in Mode 5) and the reactor

coolant

pumps were uncoupled

and

on their backseat

(which provides possible-leak

path if the Reactor

Coolant System pressurized

as it would have if all

RHR cooling were

lost for several

hours).

Plant management

and the operating staff responded

to the event in a

timely, systematic

and thorough

manner.

The resident inspector

interviewed operations

supervision

and noted

that their initial actions

included elimination or stopping all work

on control

and power supplies that might effect the remaining

RHR

pump and, further, ordering the accelerated

hookup of at least

two

core exit thermocouples

(so that core conditions could be monitored

if RHR was lost).

The resident

inspector attended plant management's

deliberations

and

action plan formulation meeting

and noted that the situation,

possible

scenarios,

and commensurate

actions

were thoroughly

discussed,

evaluated

and proper actions formulated and listed for

accomplishment.

The actions

included:

o

Establishin

containment closure

ca abilit within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> of

loss of RHR.

This action included staging of tools personnel

and coordination with radiological personnel.

Later, in. the

evening of November 3, 1988, this action was changed to

straight

away containment closure

by direction of corporate

management.

o

Providin

an ade uate

Reactor Coolant

S stem

RCS

vent

ath.

The licensee

blocked open

a Pressure

Operated Relief Valve

(PORV) and

had the Primary Relief Tank (PRT) rupture disk

physically removed to provide

a large vent path

and preclude

RCS pressurization.

o

Establishin

a contin enc

lan for o erations.

The licensee

prepared

and issued

a temporary procedure for operations

on

actions to be taken if RHR were lost.

The plan included

methods of feed

and bleed cooling and plant condition

0

prerequisites

including the blocked open

PORV, the removed

PRT

rupture disk, maintaining steam generators full (for reflux

cooling), maintaining two reactor thermocouples,

maintaining

a

charging

pump operable,

maintaining

a safety injection pump

operable,

maintaining wide range

and narrow range temporary

reactor

vessel

level indication,

and maintaining containment

closure.

The procedure

also included requirements

for

increased

monitoring of the operating

RHR pump including

trending of selected

parameters.

Licensee

management

also addressed

the paths to recovery from

the loss of the

RHR pump specifically, to repair the

damaged

pump or alternately to fill and vent the

RCS thus providing

steam generator availability.

Both paths

were accelerated

but

were predicted to require about

3 days.

The licensee

exited the event

on November 8, after the reactor

coolant

pumps were coupled

and the

RCS was filled and vented.

The repair of the

RHR pump was delayed

due to unpredicted

problems

such

as replacement

shaft runout problems (lack of

being straight)

and assembly with improper lubricant.

On

November

11,

1988, the

RHR pump was successfully tested

and

declared

operable.

The cause of the

RHR pump failure was the loosening of a nut on

the pump/motor shaft.

The nut was designed with a lock tab

washer which should

have prevented

the loosening of the nut.

One tab of the lock tab washer is turned

up against

a nut flat

and

one tab is turned

down against

a flat (or keyway)

on the

pump shaft thus preventing relative rotation of the nut and

shaft.

On the shaft of the failed pump the flat spot

had been

hand ground approximately flat as

opposed to more current

replacement

shafts

which have

a keyway machined in the shaft.

The approximate flat spot

on the shaft coupled with the fact

that the lock tab washer

was reused after

pump overhaul

(the

mechanic did not obtain

a

new lock tab washer) resulted in a

lock tab washer that did not perform its function and allowed

the nut to loosen.

Since the

pump is

a vertical shaft

assembly,

the loosening of this nut allowed the entire assembly

to move vertically downward with time.

The pump had been

successfully tested after overhaul

during the refueling outage

and

had successfully

run for about

350 pump hours.

The first

item to be

damaged

as the

pump moved vertically downward was

the lower motor bearing

lube oil sump which cracked allowing

oil to spill and

smoke

due to contact with hot rubbing

surfaces.

At the close of the reporting period the licensee

was preparing

but had not issued

a nonconformance

report on the event,

NCR

DC2-88-EM-N127.

The licensee

had determined that the event

was

not reportable

under

10 CFR 50.73 but was preparing to issue

a

voluntary

LER.

The licensee

had not completed root cause analysis at the end

of the reporting period but initial indications

expressed

by

the maintenance

manager

are that the maintenance

instructions

were not adequate.

The licensee

had not defined all actions required to prevent

recurrence

(in the absence

of a completed root cause analysis)

but had defined certain prudent actions; specifically:

o

The other Unit 2

RHR pump was partially disassembled

and the

lock tab washer installation was confirmed to be satisfactory;

o

The licensee

has prepared

a contingent design

change to stake

the nuts in place if required,

and

The licensee is preparing to examine the Unit 1

RHR pumps

and

the Unit 1 and Unit 2 Auxiliary Saltwater

(ASW) pumps which are

also vertical

pumps

and have

a similar nut locking device.

The inspectors will follow-up this item through the licensee's

LER

(2-88-15).

Com onent Coolin

Water Isolated to

RCP Thermal Barrier Cooler Of

W~ron

Unit

On November 4, 1988,

an

I8C technician isolated

component cooling

water to a Reactor

Coolant

Pump

(RCP) thermal barrier cooler for the

wrong unit.

The I8C technician

was to have worked on Unit 2 to fill and vent

a

flow indicator (2FI-90), the reactor coolant

pump thermal barrier

return flow indicator.

This work was performed

on Unit 1 instead,

which caused

an alarm in the control

room and

an automatic isolation

of component cooling water

(CCW) flow to the thermal barrier.

The technician realized

and reported his error to the control

room.

Operators

restored

cooling to the thermal barrier in accordance

with

their procedure AP-ll which requires

slow restoration to minimize

thermal

shock.

During the event

normal reactor coolant

pump seal injection was in

service,

therefore

the thermal

bar rier cooler function was not

required

and nothing detrimental

occurred to the reactor coolant

pump seals.

The I8C manager initiated a nonconformance

report

(NCR

DC1-88-TI-N216).

The underlying cause of the event

was determined

to be that the I8C technician

was dispatched

by his supervisor to

perform two jobs in sequence

(both requested

by operations).

The

first job was to check

an indicator locally at the waste

gas

compressor

in Unit 1 and then to perform an assist

step in a

surveillance

test

(STP-V-619,

Containment Isolation

Leak Valve

Testing)

Step 8.4.8 to cut in, fill, and vent FI-90 in Unit 2.

The

I&C technician

was verbally instructed

by the supervisor

and picked

a copy of the surveillance test procedure

page

from the operations

shift foreman.

For most jobs,

I8C technicians

are issued color

coded work packages,

the color accentuating

the unit to be wor ked.

As an aftermath of the event, it has

become clear that many "assist

jobs" (where

I8C action is invoked by an engineering

or operations

procedure)

do not result in a work package

being given to the

technician.

The licensee's

actions defined in the nonconformance

report were reviewed by the inspector.

The planned actions

included

counseling of the MC technician

and his supervisor

and establishing

policy that ."assist jobs" will be performed with work packages.

The licensee

determined that the event

was not reportable

under 10 CFR 50.73.

The inspectors

determined that the licensee's

actions

appeared

to be acceptable.

The effectiveness

of the licensee's

actions will be judged in the course of future inspection.

Diesel Generator

Technical

S ecification Inter retation - 24 Hour

Load Test

On November 4, 1988, the licensee's

Assistant Plant Manager for

Operations

and the Engineering

Manager discussed

with the Senior

Resident

Inspector

a technical specification interpretation which

had been

made

by the licensee.

Technical Specification 4.8. 1. 1.2.b.8 requires

a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> load test

of diesel

generators

to be performed every 18 months.

The technical

specification test requirement

as specifically written also requires

that the generator

achieve

a required voltage

and frequency within

13 seconds after the start signal.

This 13 second

requirement

had

not been

accomplished for one of the diesel

generator

units during

the 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> lead test.

However, the

same parameter is specifically

measured

monthly during a start and 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> run.

Therefore,

the

licensee

concluded that there

was

no technical

question regarding

diesel

generator operability.

The licensee

also concluded that the

technical specification requi rements

were met in that all specified

test functions

had been accomplished

in a relatively short time

period.

The resident inspector discussed

the licensee's

technical

specification interpretation with regional

management

and the

NRR

project manager.

The conclusion

drawn was that the licensee's

interpretation

was acceptable

based

on the fact that the

verification of voltage

and frequency within 13 seconds

had been

added to the 18 month surveillance test

and continued

use of the

interpretation

would not be required.

Contaminants

in Air 8 Nitro en

S stems

On November 4, 1988, the licensee

issued

a nonconformance

report,

NCR

DCO 88-TI-N125 on contaminants

found in the Nitrogen system.

The contaminants

consisted of rust and scale particles.

The

nonconformance

was generated

as

a result of a maintenance

review of

maintenance

events.

Reviewed events

included (1) an August 1, 1985,

Boric Acid Evaporator overpressurization

(and rupture disk blowout)

caused

by contamination

on nitrogen supply valve seats

which in turn

caused

in-leakage

and (2) an August 1988 nitrogen pressure

control

valve acting erratically in supplying nitrogen to the

ECCS

accumulators.

The licensee

determined

the root causes

to be oxidation during

construction

and

a design deficiency in that critical components

should contain filters.

The licensee

actions defined in the

NCR were to issue

design

changes

for the installation of filters in the boric acid evaporator

nitrogen supply, to develop

and perform a system

blowdown, to

inspect

and clean nitrogen system

components,

and to define and

initiate design action for the installation of additional filters.

The licensee

actions

are primarily in the planning stage.

A similar nonconformance

(NCR) DCO-88-OP

N116 was written on October

17,

1988,

on grit, rust,

and scale in the Instrument Air system.

The

NCR was written as

a result of finding contamination

in

instrument air piping on October 12,

1988, during modification of

the main steam isolation valve air system.

The licensee

defined

actions to prepare

a procedure to clean the system

by air blow,

inspect

a sample of air instruments,

and to analyze the contaminants

found.

At the

end of the report period,

the licensee

had not yet

determined

long term corrective action.

The licensee

I8C manager

stated that immediate operability concerns

were allayed

by the operating

experience

to date which has

successfully identified fai ling components

thr ough inservice checks.

The I8C manager stated that the identification of the problem and

the orderly performance of corrective actions

were appropriate to

the circumstances.

The inspector will follow-up the licensee's

actions through the

nonconformance

review process.

Lubricatin

Oil

S ill

On November

6, 1988, during the Unit 2 main turbine bearing oil

flush after turbine disassembly

and maintenance,

approximately

300

gallons of lubricating oil was spilled in the turbine building.

The

area affected

by the oil included the 140 foot deck with spillage

down to the 85 foot level.

The spill was caused

when

a oil return

hose

loosened

and sprayed

oil.

The condition was immediately noted

and engineers

stopped

the

flush.

The licensee

conducted

a cleanup

under the direction of an

engineer.

In addition

gA personnel

performed

an audit of the

adequacy

of the clean

up effort.

The licensee

defined the cause of the spill to be not having the

return

hose properly tied off and

a procedural failure to limit the

operating pressure

of the flush system.

The licensee

maintenance

manager

stated that an Action Request

(AR) and guality Evaluation

(gE) were prepared

to document

and track corrective actions

specifically to more securely fasten the oil hose

and to limit

system pressure.

The licensee's

recovery from this event appeared

to be largely

,verbally directed except for some specific tasks

such

as exciter

cleaning.

The inspectors

did not devote additional time to this

item since the areas

affected were not safety related.

g.

Im ro er Wire Lu s on Batter

Char ers

On November 7, 1988, the licensee

discovered

improperly sized lugs

crimped to various wires

on a safety related Unit 2 battery charger

232.

Subsequent

examinations identified the

same conditions

on

battery chargers

231, 221,

and 222.

The licensee

prepared

a nonconformance

report (DC2-88-EH-N130)

on

November

15,

1988.

Discussions

with the assistant

plant manager

for maintenance

indicated the following:

o

The improperly sized lugs were not obvious because

the involved

wire has

a thick insulation.

o

Some wires could physically be pulled out of their crimped

lugs, putting their seismic qualification in question.

o 'he condition was caused

during manufacture

by the vendor.

o

Unit 1 was checked

and found to be satisfactory.

o

Unit 2 battery chargers

have

been corrected.

o

The Unit 2 battery chargers

had functioned successfully

since

startup.

o

The licensee

had not yet determined reportability under

10 CFR 50.73 or Part

21 but would do so as part of the nonconformance

process.

The inspectors will follow-up this item through the nonconformance

process

and through the licensee

report if determined to be

reportable.

I

h.

Hissed

uadrant

Power Tilt Ratio Surveillance

Following a periodic incore/excore

nuclear instrumentation

(NI)

cross calibration,

the power

range

channels

were,

one at a time,

removed from service for adjustment.

From the time the first power

range

channel

was adjusted

on November

8, 1988, until the last

channel

was completed

on November 10,

1988, the

gPTR alarm was lit.

The shift foreman

had originally determined that the

gPTR alarm

10

annunciated

because

the adjustment

made to N-41 gave

a false

indication of quadrant

power tilt and that the alarm would clear

when all four channels

were adjusted.

Although his assumption

was

correct,

the

SFM did riot make the determination that the

gPTR alarm

was inoperable until the alarm was discussed

with the operations

manager

and operations

supervisor

on November 10.

It was then

determined that once the individual adjustment of the NI's began,

the

gPTR alarm was inoperable

since it could not perform its

intended function had an actual

quadrant

power tilt occurred.

The license initiated a nonconformance

report and will issue

a

Licensee

Event Report

(LER 1-88-27).

The licensee

determined the

root cause to be personnel

error in that the annunciator

response

manual

was not used

when the

gPTR alarm annunciated (it requires

a

quadrant

power tilt calculation or a flux map)

and that the

appropriate

determination of inoperability was not made.

The

licensee

considers that contributory causes

included inadequate

training on the

gPTR alarm and less

than adequate

procedures;

specifically that the excore recalibration procedure

should specify

that its performance

renders

the

gPTR alarm inoperable.

The inspector will review the licensee's

corrective actions in

conjunction with the review of the

LER to be submitted.

Unit 2 Safet

In 'ection

Pum

Failure

On November ll, 1988, at 12:50 a.m., operations

discovered that the

suction valve for Safety Injection (SI)

Pump 2-2 had been isolated

since 10:30 p. m. that night.

This resulted in the failure of the

pump due to a sheared

pump shaft.

The Unit was in Mode

5 and

operability of the safety injection pumps

was not required.

SI pump 2-2 had been placed inservice at 9:09 p.m. to fill three

accumulators

in accordance

with Operating

Procedure

OP B-3B: I.

At

that time,

pump suction valve 8923B was open with power removed

and

on

a clearance.

At 10:30 p.m., the clearance

was reported off for

test

(ROFTed).

Since the control

room pump position switch was in

the closed position,

when power was returned to the valve it closed.

This eliminated suction to the running SI pump.

The subsequent

heating

caused

the impeller to expand in its housing,

deform,

and

finally shear its shaft at the third element

from the inboard seal.

The motor continued to turn this portion of the shaft until the

pump

was stopped at 12:50 a.m..

The licensee initiated an Event Response

Plan which evaluated

the

cause,

reviewed the damage,

and initiated repair efforts. It was

determined that although the

pump casing

was reusable, it required

machining at the inboard seal prior to use.

As a result,

a new pump

was procured

from another plant and installed.

It was determined

that the motor did not experience

excessive

wear or heat

and could

be reused.

Testing confirmed that the overcurrent trip relays were

functioning properly, indicating that the motor did not experience

an overcurrent condition.

11

The licensee

also reviewed control

room annunciation indications

and

found that

no annunciators

"came in", and on further review of

annunciator location and design that none were expected.

Calibration checks

indicated that all inputs (motor bearing

temperatures,

stator temperature,

and seal

water temperature)

were

functioning as designed.

At the close of the inspection period,

the licensee

was reviewing the adequacy of annunciation

for the

pump.

One proposed solution was the use of a low current alarm,

which would serve the purpose of a low suction pressure

alarm and be

relatively simple to install given existing wiring.

The Technical

Review Group

(TRG) reviewing the nonconformance

report

determined

the following root causes

to the event:

o

The clearance

procedure

did not require adequate

review of the

return to service of a clearance

point with its affected

system

in operation.

o

The senior control operator failed to recognize that the

control board valve positioner

was in the closed position and

what impact it would have

on system operation

when

he removed

the clearance

tag from the valve positioner.

o

Operations

personnel

failed to adequately

monitor the

accumulator fill evolution in that it took over 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> to

recognize

the status

of the system.

The

TRG identified the following corrective actions:

o

Revisions to the clearance

procedure.

o

Addition of a low SI pump motor current alarm.

o

Counseling of the operators.

o

Generic instructions

on filling tanks.

The inspectors will follow-up licensee

actions

through the

nonconformance

report and the voluntary

LER (2-88-16).

Diesel Generator

1-3 Failed to Start

On November 12, 1988, Diesel Generator

1-3 failed to start during

testing.

The test

was

a specific test of the second level

undervoltage

relays,

the first level undervoltage

relays were

jumpered out for the test.

A licensee electrician determined the cause to be dirty contacts

on

second

level undervoltage

relay 27

HG B4.

The contacts

were cleaned

and the test

was reperformed satisfactorily.

Licensee

records

show

that the relay had been

removed

on September

21, 1988, for periodic

calibration.

The procedure

used required contact cleaning

and an

continuity check at that time.

0

12

The licensee's

Nonconformance

Report

NCR DC2-88-TN-N132 was in draft

at the close of the inspection report.

The licensee

had not

resolved

the reason for dirty contacts

occurring

on November 12,

1988.

Further,

the licensee is preparing

a special

report required

by

technical specifications

to report all valid and non-valid failures

to start.

The residents will follow-up the licensee's

action

through review of the nonconformance

and special

report process.

Boron In'ection Tank Relief Valve Heat Tracin

On November 18,

1988, during a routine walkdown, the system engineer

for the chemical

and volume control

system

observed that thermal

insulation over heat tracing

on the Unit 1 Boron Injection Tank

(BIT) relief valve (RV) was not properly restored following

maintenance.

Additionally, the heat tracing

had been lifted away

from the valve approximately 4" to 6" to facilitate

RV maintenance

performed during the Unit 1 refueling outage earlier this year.

Temperature

measurements

of the relief valve subsequent

to the

discovery found the temperature

to be 130 degrees

F,

15 degrees

F

less

than the Technical Specification (TS) 5.4.2 required

145

degrees

F (which maintains

boron in solution).

It was determined

by the Onsite Project Engineering

Group

(OPEG)

that 130 degrees

would not have precipitated

enough

boron to have

prevented

the relief valve from lifting at its designed

pressure.

The licensee

also determined that the heat tracing'TS 3.5.4.2 did

not apply to the

RV since it is not a part of the BIT flow path

piping.

The root cause

was determined to be

a failure to provide separate

instructions for the removal

and reinstallation of heat tracing and

insulation during the Unit 1 outage in conjunction with other work.

The licensee

revised its practices prior to the Unit 2 outage

and

supplied separate

work orders for the installation

and removal of

heat tracing and insulation

and for the work performed

on

components.

Inadvertent Start of Auxiliar

Feedwater

Pum

s

On November 21, 1988, the licensee

made

a 4-hour non-emergency

report

due to the inadvertent start of Unit 2 auxiliary feedwater

system

pumps.

The pumps started

due to a start signal

from the newly installed

AMSAC system (Accident Mitigation System Actuation Circuitry) during

testing of the newly installed system.

Testing of the system

had

been ongoing since October 30, 1988, but had not caused

actuation

since the auxiliary feedwater

(AFW) had been de-energized

for other

refueling outage

reasons.

When operations

personnel

made the

AFW

system available

on November

21, testing then induced

a start of the

now energized

equipment.

The plant computer

(P-250)

had

been taken

out of service for modifications about one-half

hour prior to the

13

pump start.

The

AFW was

made available

and started

but was not

noted

by operators

for about another one-half hour until the P-250

was restored

and the alarm typewriter started printing an alarm.

In discussion with the

I8C manager

and the plant operations

manager,

the following was established:

o

The

AFW pumps were .lined up on recirculation to the condensate

storage

tank, therefore

no damage

was incurred.

o

The motor driven pumps started.

The steam driven pump had its

steam admission valve open it did not start

due to the absence

of steam in Mode 5.

o 'he

steam generator

blowdown did not isolate.

This feature

was

part of the intended design.

Subsequent

examination

showed the

wiring design to be in error.

Although this was subsequently

corrected, it pointed out a separate

problem according to the

I8C manager.

Specifically the problem was that test

requirements

were not specified

by PG8E design engineers.

The

test requirements

are, deduced

by test engineers

at the site

based

on the modification drawing logic.

The I8C manager

further stated that in this case

the drawing circuitry as

described

in modification drawings did not describe

a logic

where

steam generator

blowdown would be isolated.

Therefore,

test engineers

did not specify it as

a feature to be tested.

The licensee's

response

to the maintenance

team inspection

indicated that, in the future, test requirements

would be

specified

by design engineers

and that details of the test

methods

would be invoked by plant staff personnel.

The inspectors will follow-up licensee

actions through the

nonconformance

and event report process.

Residual

Heat

Removal

Water

Hammer

On November 23,

1988,

a water

hammer

was noted in the control

room

concurrent with the start of an Residual

Heat Removal

Pump in Unit 1

dur ing a routine surveillance test.

Operators

performed

a walkdown

and noted

no damage.

Subsequently,

walkdowns were performed

by

engineering

and again

no damage

was noted.

Engineering personnel

conducted

a series of pump starts with several

personnel

stationed at various points along the

RHR system.

The

engineers

noted decreasing

energy in the water

hammer effect with

subsequent

pump starts

and noted the location of the loudest noise

to be near

the suction check valve to the Refueling Water Storage

Tank (RWST).

The licensee

engineers

developed

two theories

regarding the cause of

the water

hammer,

one involving entrapped air in long horizontal

runs

and

one involving temporary opening of the

RWST check valve on

starts

due to suction

dynamic action.

The licensee

engineers

have

referred the matter for further study by a general office group

referred to as the water

hammer task force.

The licensee

engineers

do not consider the energy demonstrated

to be

an operational

concern

based

on engineering

judgement.

A second

similar water

hammer event occurred

on December 1, 1988,

as noted in

paragraph 4.s..

The inspectors will follow-up this as

an open item, since the

licensee

does not consider the item to be a nonconformance

(Follow-up Item 50-275/88-31-01).

Containment Ventilation Isolation

CVI

Event in Unit 2

On November 12,

1988, the licensee

made

a 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />

non-emergency

report to the

NRC due to a containment ventilation isolation (CVI)

event in Unit 2.

The event occurred during planned calibration of plant ventilation

radiation monitor

2 RM-14B.

The procedure calls for lifting leads

to prevent

a CVI.

The cause of the event was determined to be that

the lifted leads

were lifted and taped

away in a manner which

allowed the lead terminal

lugs to come into contact

and complete

a

CVI signal

when, later in the procedure,

fuses

were pulled.

The inspectors will follow-Up the licensee's

corrective action

through the event report to be issued.

Unit 2 Low Tem erature

Over ressure

Protection

S stem Actuation

On November 25, 1988, while in Mode 5, Unit 2 experienced

four low

temperature

overpressure

protection

(LTOP) system actuations.

The

first actuation occurred at 6:20 a.m. following filling and venting

the

RCS while operators

were attempting to pressurize

to 390 psig to

run the reactor coolant pumps.

The lift involved pressurizer

power

operated relief valve PCV-456, which at low temperatures

is set to

liftat 435 psig hot leg pressure.

The other three lifts occurred

within the span of four minutes while operations

brought the

RCS to

400 psig to perform

RCS leakage

inspections.

As a result of these

actuations,

the licensee

is required

by technical specifications to

submit

a special

report.

The hot leg pressure

transmitters

are 0-3000 psig instruments

accurate

to 3X or 30 psig;

and although the controls for PCV-456 and

the control

room instruments

are fed from one transmitter,

PT 403,

the process

loops are separate.

In this case,

the instrumentation

in the control

room read approximately

25 psig lower than the

controls for PCV-456 were sensing.

As a result,

operators

were

operating

much closer to the liftpoint. than perceived.

In

addition,

a contributing cause to the first lift, as determined

by

the operations

manager,

was operator inattention.

A contributing

cause in the second set of lifts, as determined

by the operations

manager,

was lack of procedural

guidance

on the

use of the seven

means of control

room indication supplied by two pressure

15

transmitters.

The inspector will follow the determination of

corrective action in follow-up of the special

report to be

submitted.

Unit 2 Containment Ventilation Isolations

On November 26,

1988, Unit 2 experienced

two containment ventilation

isolations

(CVIs).

The first CVI occurred

when radiation monitor

2-RM-148 spiked high.

The cause

was determined to be

a detector

tube failure.

The second

CVI occurred during removal of the failed

detector

from service for repair.

Since the original CVI signal

had

been reset

and ventilation was in normal

mode the act of lifting

leads to remove the failed high radiation monitor caused

the

electrical contact to be broken and then

made

up again (during the

physical act of lifting a round termination lug off the termination

post).

The recontact provided

a second "spike" to the logic circuit

causing the

CVI actuation.

The inspectors will follow-up licensee

actions

through the

LER

process.

Unit 1 Containment Air Particulate

Monitor

RM-12

Ino erable

On November

26,

1988, instrumentation

and controls (I8C) technicians

discovered

the sample

supply isolation valve for RM-12 closed.

It

was determined

by the licensee that it had been closed

on or

sometime

since October ll, 1988,

when

IBC had last performed routine

testing.

Either

RM-12 or the containment

fan cooler condensate

monitoring system are required to be operable

as part of the reactor

coolant system

(RCS) leakage detection

system (Technical Specification 3.4.6. 1).

The condensate

monitoring system

was not

put in service during this time frame and was therefore not used to

detect

RCS leakage.

The licensee's

determination of root cause

and corrective action

will be followed up by the inspector in response

to the

LER to be

issued

on this subject.

Electrical Transient Resultin

in En ineerin

Safet

Features

Actuations

On November 28, 1988, at 8:08 p.m.,

when, Unit 2 was in Mode 4 (Hot

Shutdown)

a temporary loss of power to vital instrument

AC

distribution panel

PY-22 resulted in the actuation of several

Engineered

Safety Features

(ESF)

as well as several

other

actuations.

Actuations included CVI, fuel handling building

ventilation mode shift, pressurizer

heater trip, steam

dump closure,

and letdown isolation.

At the end of the report period, the cause of the electrical

transient

was still under investigation.

The inspector will

follow-up the event through review of the

LER to be submitted

on the

event.

16

s.

Second

RHR Water

Hammer

On December

1, 1988, Unit 1 experienced

a second

RHR water

hammer

when the

RHR pump was started for surveillance testing.

Paragraph

4.m.

regarding the

RHR water

hammer event of November 23, 1988,

provides further discussion.

5.

Maintenance

62703

The inspectors

observed portions of, and reviewed records

on, selected

maintenance activities to assure

compliance with approved procedures,

technical specifications,

and appropriate

industry codes

and standards.

Furthermore,

the inspectors verified maintenance activities were

performed by qualified personnel,

in accordance

with fire protection

and

housekeeping

controls,

and replacement

parts were appropriately

cer tified.

a.

Residual

Heat

Removal

Pum

2-2

As described

in the previous section,

on November 3, 1988, the lower

bearing

on

RHR pump 2-2 failed shortly after an attempt

was

made to

start the

pump.

Details of the initial failure and subsequent

problems

are contained in section 4.

The inspector

observed

the

following maintenance activities

on the pump; portions of the

as-found inspection, as-left shaft runout measurements,

and portions

of the motor reassembly.

The activities observed

were found to be

performed in accordance

with appropriate

procedures.

It was noted

that the activity was observed

by quality control inspectors

and the

maintenance

department

manager.

b.

Unit 1 Centrifu al Char in

Pum

1-2 Lube Oil Leak

On November 17,

1988, during a routine walkdown, the inspector

noted

that centrifugal charging

pump 1-2 (CCpp 1-2), which was in

operation,

had

a significant amount of lube oil under

and around the

pump.

No specific leak point was apparent,

although it appeared

to

come from the area of the

pump outboard bearing.

The condition was

noted to the Unit 1 shift foreman

and the maintenance

manager.

Lube Oil

S stem - A Brief Descri tion of 0 eration

In order to understand

the issues

in this section of the report

a

brief description of the operation of the charging

pump bearings

lubrication oil system is necessary.

Specifically, two pumps take

suction from the lube oil (LO) reservoir;

the

CCpp shaft driven

"main"

LO pump and

a motor driven "Auxiliary" LO pump.

The two

pumps supply

a header

which supplies

system flow and bypass

flow.

Bypass flow is controlled by a relief valve which is designed to

maintain system pressure

between

10 and

12 psi.

Main flow goes

through the lube oil cooler (cooled

by component cooling water),

through

a filter and to a header.

The header

supplies the inboard

and outboard

pump bearings,

pressure

instrumentation

and controls.

The pressure

instrumentation

and controls include

a local indicator,

a low lube oil pressure

annunciator,

a lube oil pressure

CCpp start

permissive,

and start

and stop pressures

for the Auxiliary LO pump.

The system is designed

such that on a control

room start,

the

Auxiliary LO pump starts

and raises

lube oil pressure

from

essentially

zero psig.

The lube oil pressure

permissive

(PS

295/296) allows the

CCpp to start

when pressure

reaches

the setpoint

of about

9 psig.

The Auxiliary LO pump and the Main

LO pump build

up system pressure

to a setpoint which turns off the Auxiliary pump

(PS 293/294).

System pressure

should then reach

an equilibrium

based

on the setting of the relief valve which acts

as

a pressure

regulating device.

Ins ection:

The inspectors

investigation of the leak revealed

a number of

concerns

described

below:

o

The inspector

reviewed action requests

and determined that

there is long history of charging

pump lube oil system problems

with a number of unresolved

issues.

Starting in March 1983

problem reports chronicle pressure

switch setpoint problems,

oil pressure

outside manufacture

recommendations,

excessive

auxiliary

LO pump cycling and lube oil leaks.

One quality

evaluation

was

open at the time of inspection.

It was opened

on November 16,

1986,

and identifies problems

on

CCpp 1-2 and

CCpp 2-2 such

as excessive

clearances,

leaking valves,

lube oil

quality and instrument setpoints.

Responsibility

and due dates

on the

gE had changed

and when reviewed by the inspector the

target date

was September

1989.

This appeared

to be

an example

of a lack of timely corrective action

and

a lack of clear

problem ownership which was identified to the licensee at the

management

SALP meeting held in Walnut Creek, California,

on

October 26,

1988.

o

Instrumentation

and Relief Valve setpoints

were inadequately

controlled.

The

pump manual

requires that pressure

to the

pump

bearings

be maintained

between

10 and 12 psig.

The system

engineer,

following questions

from the inspector,

found that

the relief valve, which acts

as

a lube oil system pressure

regulator

was set to 19 and 20 psig, respectively for the two

charging

pumps,

by the periodic maintenance

procedure.

As a

result,

system pressure

has not been controlled by the relief

valve since with the valve fully closed

main

LO pump discharge

pressure

is between

12 and

17 psig.

In addition, the Unit 1

and

2 CCpp start permissive setpoints

were different and

documentation

did not definitely established

what the

appropriate settings for the permissive were.

As a result,

the

LO system

has operated consistently outside the

recommended

10

to 12 psig band.

o

The leak on

CCpp 1-2 had received little attention since the

leak was identified by the licensee.

The leak was identified

on August 23, 1988,

on an Action Request.

The inspector

brought the matter to the maintenance

managers

attention

on

18

November 18,

1988.

At that time,

no actions'o

analyze or

correct the situation

had been performed.

The amount of oil added to pumps

and motors is not trended.

An

informal log at the auxiliary building auxiliary operator

panel

was

used to track how much total oil was put into various

pumps.

However, the log did not specify exactly where the oil

went (e.g.

the log indicated that

3 gallons of oil had been

added to the

CCpp on October 25, 1988, did not specify where it

was added;

the pump, the speed increaser,

or the motor).

In

addition, through interviews with the auxiliary operators

(AOs)

it was determined that not all

AOs were aware of the log.

These

concerns

were discussed

with the assistant

plant manager for

maintenance

on November 29,

1988.

As a result of these discussions

a system engineer

was given the task of establishing

what problems

existed

and what corrective actions

were necessary.

In addition,

the work planning manager stated that

a procedure in draft would be

revised to include actions to be taken following the discovery of'n

oil leak similar to the actions

being specified in the draft for a

boron leak.

These actions

include

a timely engineering

walkdown and

evaluation.

Finally, the plant manager

committed in the exit

meeting to consider

implementing

pump and motor oil consumption

trending.

The inspectors will follow-up the licensee's

actions in

the course of future inspections.

No violations or deviations

were identified.

6.

Surveillance

61726

By direct observation

and record review of selected

surveillance testing,

the inspectors

assured

compliance with TS requirements

and plant

procedures.

The inspectors verified that test equipment

was calibrated,

and acceptance

criteria were met or appropriately dispositioned.

a ~

Auxiliar Saltwater

Pum

2-2 Baseline

Performance

Test

On October 28, l988, the inspector

observed portions of the

performance of the Auxiliary Saltwater

Pump 2-2 baseline

performance

test

(STP P-7A).

The test

was performed to determine

a new pump

curve for the

ASW pump following impeller replacement.

Except for

the one discrepancy

discussed

below, the test

was performed in

accordance

with the procedure.

The procedure

requires

the reading of an annubar flow gauge to

determine flow with varied heat exchanger outlet valve position

(steps

8, ll to 8. 15).

The inspector, observed that the annubar

was

fluctuating erratically + 5X of full scale.

The test engineer,

after attempting to throttle the gauge isolation valves to minimize

the oscillation, observed

the gauge for between

30 and

60 seconds

to

visually determine

a mean flow value.

This reading

was not obtained

in accordance

with procedure

AP C-353, "Administrative Procedure

Dealing With Gauge Oscillations During the Performance

of ASME

Section

NI Required Tests",

issued

September

23,

1988.

The

0

19

procedure

requires that if a gauge is oscillating irregularly

greater

than

2X of the midpoint reading but not exceeding 10'f

gauge

range,

to "..take

5 spot readings at 10 second intervals,

sum

the

5 readings

and divide the

sum by 5 to obtain

an average

reading."

In addition, the procedure

also requires that

an action

request

should

be written which was not done.

The failure of the

test engineer to follow procedure is an apparent violation (Item

50-323/88-29-01).

The above incident was preceded

by a history of enforcement actions

dealing with improper test instrument reading.

A similar instance

was observed

by an inspector

on February 10,

1988 when fluctuations

of flow of greater

than that allowed in the procedure

were observed

when testing

a Containment

Spray

pump 1-1.

-This resulted in a

notice of violation (Inspection Report 50-275/88-04) for failure to

=

obtain test reference

values within tolerances

specified in ASME XI.

In response

to the notice of violation, the licensee

committed to

write an an administrative procedure for reading

and interpreting

test instruments

by July 1, 1988.

An inspection in September

found

that the licensee

had not implemented this commitment.

This

resulted in a notice of deviation (Inspection Report 50-275/88-25)..

Procedure

AP C-3S3, which implemented the licensee's

original

commitment

was issued shortly after the inspection

(Open Item

50-275/88-25-01,

closed).

The inspector discussed

the system engineer's

failure to follow the

procedure with the assistant

plant manager for technical

services.

Three issues

were discussed.

First, from interviewing the system

engineer,

the inspector determined that he had been

unaware of the

issuance

of procedure

AP C-3S3

and that a determination of why he

had been

unaware

and corrective actions to prevent recurrence

was

needed.

Second,

the inspector

requested

the licensee

provide the

technical

basis for the sampling method

used in procedure

AP C-3S3.

Finally, the inspector

expressed

concern that the issue of gauge

reading

had been handled slowly and was another

example of untimely

resolution of identified problems discussed

in the

SALP report.

Following the discussion

a nonconformance

report was initiated.

The technical

review group

(TRG), which convened to review the

nonconformance

report determined that the engineer

had not been

informed nor trained on

AP C-3S3, although it was his

own supervisor

who had written the procedure.

Further, the

TRG determined that no

formal mechanism existed to notify and train plant engineering

personnel

of new and revised administrative procedures.

Corrective

actions identified by the

TRG included establishing

a formal program

to accomplish training in new and revised procedures

for plant

engineering

and to assess

the

need for such

a program in other

departments.

The inspector will review these corrective actions in

follow-up of the notice of violation enclosed in this report.

At the end of the report period, the licensee

had not provided the

inspector with a basis for the averaging

technique

described

in AP

C3S3.

This was discussed

in the exit meeting

and the plant manager

20

committed to include the basis in their response

to the notice of

violation enclosed

in this report.

b.

Continuit

Testin

of Feedwater Isolation Slave

Rela

On December

2, 1988, the inspector

observed

the testing of the train

"A" solid state protection

system

(SSPS)

feedwater isolation slave

relay (K601A) for Unit 1.

Three attempts

were required to actuate

K601A (which, is normally closed

and opens

on an actuation signal).

During the first two attempts,

the relay failed to open.

These

first two attempts

were performed by the senior control operator

and

an auxiliary control operator.

The third attempt

was witnessed

by

the shift foreman

and supervising

instrumentation

and controls (I&C)

technician.

To test slave relay K601A, test switch S801A is taken from "normal"

to "push-to-test."

This actuates

test relay K801A which provides

a

bypass circuit which ensures

that the feedwater isolation valves

remain

open

when

K601A is tested.

In addition,

K801A provides

a

permissive

which allows S801A,

when depressed,

to actuate

K601A. It

was determined

by the

I&C technician that the set of contacts

which

provide this permissive did not make

up.

The determination

was

based

on indirect evidence

as

opposed to direct observation of the

contacts

or evidence

which ruled out failure of the slave relay.

The evidence

included:

o

K801A made

a buzzing all three times which, per the

I&C

technician,

indicates that the relay had not rotated completely

when it actuated.

o

Visual observation

by the

I&C technician

on the third attempt

that

K801A had not rotated completely.

o

The slave relay

K601A did not actuate at all the first two

tries

and rotated fully the third try indicating it had not

received

any power on the first two attempts.

o

A history of test relay problems

and

no history of slave relay

problems.

The inspector discussed

the test with the

I&C manager

and concurred

that the licensee

determinations

appeared

to be appropriate.

One violation was identified as noted above in paragraph

6. a..

8.

Radiolo ical Protection

71707

The inspectors periodically observed radiological protection practices

to

determine whether the licensee's

program was being implemented in

conformance with facility policies

and procedures

and in compliance with

regulatory requirements.

The inspectors verified that health physics

supervisors

and professionals

conducted

frequent plant tours to observe

activities in progress

and were generally

aware of significant plant

activities, particularly those related to radiological conditions and/or

21

challenges.

ALARA consideration

was found to be an integral part of each

RWP (Radiation

Work Permit).

Removal of Scaffoldin

From Unit 2 Containment

The inspector

observed

health physics

(HP) practices

in the removal

of scaffolding from the Unit 2 containment while the Unit was in Mode

5

on November 6, 1988,

between approximately 9:30 p.m.

and midnight.

Scaffolding was delivered to the containment

equipment

hatch at the

140'evel

from the 115'evel

by PG8E General

Construction

(GC) personnel.

The scaffolding and clamps were then wiped down by the

GC personnel.

The

wipes were then frisked by

HP personnel

monitoring the evolution.

The

scaffolding and clamps

were then passed

out the containment

equipment

hatch,

over

a walkway of herculite,

which had been laid down prior to

opening the hatch; to a holding area.

The equipment

remained controlled

inside

a surface contamination

area

and did not pass

from one level of

contamination control to another.

The inspector

interviewed

one of two HP technicians

monitoring the work.

The

HP technician stated that all wipes were being frisked to determine

the relative contamination of the scaffolding.

The technicians

acceptance

criteria was 10,000

dpm.

The technician stated that

no

contamination greater

than the acceptance

criteria.

The technician also

indicated that the intent was not to decontaminate

scaffolding but to

identify scaffolding with relatively high contamination.

The inspector

discussed

the work with the radiation protection

foreman for containment.

His understanding

of the process

concurred with that of the technician.

In addition,

he stated that the scaffolding would be bagged

and frisked

before being taken outside the Radiological Controls Area for storage

as

radioactive material.

He noted that this was the practice

used in three

previous

outages.

The

RP foreman stated that scaffolding taken

from a

hot particle zone

(HPZ) received inspection

and either decontamination

or

bagging prior to removal

from the

HPZ.

He noted that to his knowledge

no

scaffolding was at that time being removed from an

HPZ.

The inspector also interviewed the security guard

who was present

when

the equipment

hatch

was opened.

He stated that the laydown area

and path

to containment

had

been established

prior to opening the hatch.

The inspector discussed

with and observed

GC personnel

transfer

scaffolding from the 115'evel

to the 140'evels

At the time of the

inspection it was observed that no scaffolding was being disassembled

and

that scaffolding being transferred

were parts

staged for removal outside

the bioshield

on the 115'evel.

The i.nspector

found practices of HP and

GC to be acceptable.

Additionally, the following morning, the radiological protection manager

was requested

to independently

assess

whether radiological practices

in

the movement of the scaffolding were proper.

His subsequent

response

after

a survey of radiological

personnel

involved in the job was that

radiological practices

were proper,

The request to the radiological

protection

manager

was

made in response

to the fact that

some workers

involved in the job had expressed

concerns

regarding the adequacy of

controls exercised.

22

No violations or deviations

were identified.

9.

Ph sical Securit

71707

Security activities were observed for conformance with regulatory

requirements,

implementation of the site security plan,

and

administrative procedures

including vehicle and personnel

access

screening,

personnel

badging, site security force manning,

compensatory

measures,

arid protected

and vital area integrity.

Exterior lighting was

checked during backshift inspections.

No violations or deviations

were identified.

10.

Licensee

Event

Re ort Follow-u

92700

aO

Status of LERs

d

The

LERs identified below were also closed out after review and in

selected

cases

follow-up inspections

were performed

by the

inspectors

to verify licensee corrective actions:

Unit 1:

88-14,

88-20

Unit 2:

87-26, 88-04, 88-08, 88-11, 88-12

b.

0 en

Unit 2 Ino erable

Reactor Cavit

Sum

Level Indicator

LER

2"88"13"00

On November 14, 1988, the licensee

issued

LER 2-88-13-00 which

discussed

the Unit 2 inoperable reactor cavity sump level

(RCSL)

indicator.

The level indicator was found to be inoperable during

the recent refueling outage

due to the isolation of it's instrument

air supply.

The

RCSL indicator is part of the technical specification 3.4.6. 1 reactor coolant leakage detection

system which

includes the'ontainment

structure

sump, the containment particulate

and gaseous

radiation monitors

RM-11 and

RM-12, and the Containment

Fan Cooler Collection Monitoring System

(CFCCMS).

The inspector

reviewed the "Analysis of Event" portion of the

LER.

In a review of the operability status of the

CFCCMS and

RM-11 and

RM-12, the submittal stated that "Except during routine testing of

the radiation monitors, all channels

were available to perform their

intended function.

The above two monitoring systems

remained

operable

and would have indicated increased

signs of RCS leakage,

had there

been any."

The inspector

found approximately five

corrective maintenance

work orders

on RM-ll and RH-12, indicating

that the radiation monitors

had been out of service for other than

"routine testing."

In addition,

a review of the inspectors

notes

showed that the radiation monitors

had been inoperable

from

September

28 to October 1, 1987.

The licensee

was requested

at the

exit meeting to provide the out of service times for RM-ll and

RM-12.

23

In addition, the

LER is misleading in that the

CFCCHS was

made

operable

as

a compensatory

action only when

RM-12 was taken out of

service.

The analysis

submitted did not fully discuss

the adequacy

of the remaining leakage

detection

systems.

C.

These questions

were discussed

with the Regulatory Compliance

Supervisor

who committed to submit a revised analysis.

This item is

considered

an unresolved

item (Item 50-323/88-29-02)

pending

resolution of the inspectors

questions.

0 en

Emer enc

Core Coolin

S stem

ECCS

Not Vented Within

Technical

S ecification

Re uired Limit

LER 2-88-06

The

LER issued July 5, 1988, specified,

as corrective actions,

revision of Administrative Procedure

AP C-3Sl " Surveillance Testing

and Inspection."

The revision was to emphasize

the timely closure

of completed recurring surveillances

so that a new test

can be

scheduled.

At the end of the report period, this revision had not

been

completed

(a period of five months).

At the exit meeting,

the

inspectors

discussed

the ongoing concern with lack of timely

corrective action.

This item will remain open.

(Closed

Inadvertent Autostart-of Diesel Generator

1-3

Due to

Personnel

Error

LER 2-88-12-00

The licensee

submitted

LER 2-88-12-00

on November 8, 1988.

The

LER

discussed

'the inadvertent start of a diesel

generator

when a

maintenance

contractor for the Unit 2 outage tried to obtain power

to test

an auxiliary transformer relay from the startup transformer

and energized its differential relay.

The inspectors

found the root cause

determination corrective actions

to be acceptable.

This was

an example where personnel

did not

recognize that instructions

were not adequate

and did not stop their

activity.

This issue

was the subject of discussion

in the

SALP

meeting (Inspection

Report 50-275/88-30).

The inspectors will

continue to monitor the'licensee's

progress

in this area

(LER

50-275/88-12-LO,

Closed).

No violations or deviations

were identified.

ll.

Reactive

Ins ection

a 0

Containment

Tem erature

Tem orar

Instruction 2515/98

CLOSED

In response

to high containment

temperatures

affecting safety

related

components at a number of plants,

a Temporary Instruction

(TI 2515/98,

issued

June

20, 1988)

was issued requiring an

inspection of containment

temperatures

and monitoring systems.

The

TI included an attachment that listed eight questions.

The

inspectors

findings for the questions

are included as

an attachment

to this report.

In summary,

the inspector

found that the licensee's

temperature

monitoring was acceptable

to meet design basis

accident

assumptions.

The licensee's

efforts to formalize its procedures

for monitoring

and evaluating

peak temperature

experienced

during

a fuel cycle were

found to be prudent

and will be followed through routine inspection.

Effectiveness

of ualit

Assurance

Ins ections

36700

A review was performed of a limited sample of guality Support

surveillance

inspection.

guality Support (gS), the onsite division

of guality Assurance,

performs periodic surveillances

on all aspects

of plant activities in accordance

with gS procedure

gS-4.

The

inspector

reviewed surveillances

gS 88-0562,

0715,

and 0746.

All

three were walkdowns of containment penetration

manual isolation

sealed

valve checklists.

Although a number of discrepancies

between

the checklist

and

as-found condition were noted in the three surveillances,

none of

the survei llances

adequately

discussed

the cause of the

discrepancies

or invoked adequate

tracking of corrective actions.

S 88-0562

The

gS inspector identified f'ive discrepancies

with the inside

containment isolation valve sealed

valve checklist

OP K-10B1,

including valves in the positions other than specified in the

checklist

and missing seals.

The "Disposition/Conclusion" section

of the surveillance

stated:

I

"These valve positions

are satisfactory for the

mode

we are

currently in, but must be corrected

before entry to Mode 4."

r

An independent verification by the inspector determined that the

plant was in Mode

6 "Core Alterations" at the time of the

gS

inspection.

In this mode

TS require

a level of containment

isolation, although not as stringent

as the

Modes

1 to 4 alignment.

The operations

department

was controlling the

Mode

6 containment

isolation with a clearance

and

OP K-10B1 was "inactive" (essentially

not controlled).

The inspector determined that gS had not verified

that the discrepancies

identified agreed with the containment

clearance

although the resident inspector

independently

made this

verification.

The

gS effort identified seal

valve "discrepancies"

from a list that was not applicable.

S 88-0715

This surveillance

documented five discrepancies

of outside

containment isolation valve checklist

OP K-10B2.

The disposition

stated

"The above

must be corrected before entry to Mode 4."

In an

interview with the

gS inspector,

the inspector

learned that

gS had

handed

the list of discrepancies

to the Unit 2 shift foremen

(SFM)

for action.

In addition,

no action

was taken to formally follow-up

the correction of the discrepancies

and to determine

the cause.

The

inspector

independently

discussed

the

gS list with the

SFM and

25

discovered that the

OP K-1082 valve alignment

was in process.

Four

of the points

had yet to be signed off.

The other

two points

involved end caps

and plugs not installed.

On follow-up, after

discussions

with the resident inspector,

gS determined that the

appropriate

end caps

were installed

and the original

gS finding had

been erroneous.

This is another

example where

gS did not perform a

verification that the applicable controls were, in fact,

functioning.

S 88-0716

This gS inspection resulted

from discussions

the resident inspector

had with the

gS supervisor

as

an effort to formally resolve

discrepancies

identified in the previously discussed

surveillance

gS-88-0715.

The

new report (gS-88-0716)

stated

"Deviations listed

previously have

been corrected with the exception of valve

AIR-S-2-200."

Again, the deviation was not tracked nor did gS

indicate in the surveillance report that the valve had not been

closed

by operations

or that

Op K-10B2 had not been completed

by

operations.

As a result of the findings discussed

above,

the resident

inspector

discussed

weaknesses

identified in the conduct of gS survei llances

with the

gS supervisor.

Specifically, the inspector considers that

if a "deviation" is found by gS, its validity should

be verified,

the cause of the deviation should

be identified,

and formal

corrective action should

be taken.

If these final steps

are not

taken,

then the effectiveness

of the

gS surveillance

program of

identifying quality problems

and initiating lasting corrective

actions is limited.

Mhile it was noted that gS has accomplished

the

above in some of their recent inspections

(such

as the Penetration

63 issue during the Unit 1 second refueling outage

and the Auxiliary

Saltwater impeller issue),

the concept that inspections

should

be

conducted to a meaningful conclusion

appears

to need additional

attention.

As a result of the discussion,

the

gS supervisor initiated a guality

Evaluation

on the issue of gS surveillance follow-up.

The inspector

will evaluate

the adequacy

of the corrective actions in a future

inspection.

12.

Unresolved

Items

Unresolved

items are matters

about which more information is required in

order to ascertain

whether they are acceptable

items,

items of

noncompliance,

or deviations.

An unresolved

item disclosed

during this

inspection is discussed

in Paragraph

10.b. of this report.

On December

12,

1988,

an exit meeting

was conducted with the licensee's

representatives

identified in paragraph

1.

The inspectors

summarized

the

scope

and findings of the inspection

as described

in this report.

C

26

ATTACHMENT TO INSPECTION

REPORTS 50-275/88-31

and 50-323/88-29

INFORMATION FOR TI 2515/98

CONTAINMENT TEMPERATURE SURVEY

1.

2.

3.

Plant

Name:

Diablo Canyon Units 1 5 2

Unit 1

Docket Number:

50-275

Unit 2

Docket Number:

50-323

What are the average

containment

temperatures

during operations

as

recorded

by the licensee?

Note:

We are interested

in the peak operating

temperatures

during the hottest

summer months.

Discussions

with the Operations

Department indicated that Diablo Canyon

normally operates

with containment

temperatures

below 110 degrees.

The

inspector

reviewed containment temperature

history data provided by plant

engineering

which confirms this for the months of April to October 1987

and April to September

1988.

The temperatures

provided were the

technical specification required daily recorded

average of four

containment

temperature

monitors.

The average

containment temperatures

varied for these

summer

months

from between

94 and 103.3 degrees

F.

The

hottest temperature

recorded

was 108.4 degrees

in October

1987 for Unit

l.

Diablo Canyon rarely experiences

high ambient temperature

conditions

due

to the coastal

climate.

During the

summer months,

coastal

fog covers the

site for most of the day,

keeping temperatures

in the 60's

and 70's.

Infrequently, inland winds will warm the coast

as in October 1987.

The

containment is cooled by five containment

fan cooler units

(CFCUs), which

are cooled

by the component cooling water system which is cooled by the

auxiliary salt water system

(ASWS), the ultimate heat sink, which take

suction from the Pacific Ocean.

The ocean

temperature

normally remains

below 64 degrees

F.

The

ASWS and

CFCUs are sized for accident conditions

and at normal temperatures

can easily handle containment

ambient

conditions.

Containment

temperature

at which the plant is licensed to operate (i.e.,

operating

temperature

specified in the

FSAR).

Plant Technical Specification 3.6.1.5 requires that average

containment

temperature

shall not exceed

120 degrees

F in modes

1 through 4. If 120

degrees

F is exceeded

for over eight hours the licensee is required to be

in hot standby in the following six hours

and cold shutdown in the

following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.

To ver ify containment

average

temperature

the

licensee

is required to take

an average of four monitors.

The monitors

are located inside the bioshield between the steam generators,

o'utside

the bioshield

on the

same level,

on the refueling deck level,

and on top

of the steam generator

missile barriers

away from the steam generators.

The basis for Technical Specification 3.6. 1.5 is to ensure that the

overall containment

average air temperature

does not exceed the initial

temperature

condition assumed

in the safety analysis for a loss of

coolant accident.

These initial conditions for the

LOCA analysis

are

described

in FSAR Table 6.2-4.

'eview the temperature

readings

and provide your assessment

as to whether

or not you believe the average

temperature

readings

accurately reflect

containment conditions,

or if there is a significant difference,

due to

S

g

~

27

temperature

sensor

location or stratification of containment

atmosphere

which could produce hot spots.

The average

temperature

readings

appear to provide an accurate

containment

average

temperature

in that it is a simple assessment

of what

is the average

temperature

of the containment air volume, providing an

energy input for the

LOCA calculation.

The containment

does

have "hot

spots" which are not accounted for by the average

temperature.

Mhat temperatures

are

used

by the licensee

in its equipment environmental

qualification program when calculating the remaining qualified lifetime

for all equipment inside containment,

and are these

temperatures

consistent with temperatures

experienced?

Post-LOCA environment temperatures

are based

on the initial ambient

average

temperatures

of 120 degrees.

In addition, the equipment life

calculations

are

based

on 120 degrees

at the component.

Currently, the

licensee is establishing

a program of monitoring the peak temperature

experienced

at all environmentally qualified equipment locations inside

containment.

This involves attaching temperature

recording stickers

(which record the highest temperature

to which they are exposed) at the

beginning of a fuel cycle and removing them during the next refueling

outage.

The results

are then forwarded to Engineering for analysis.

At

the time of this report

a final analysis

had not been performed for

either Units 1 of 2.

Preliminary data indicates that

some equipment is

exposed to greater that 120 degrees,

such

as equipment

on top of the

pressurizer.

The solenoid valves,

which operate

the pressurizer

power

operated relief valves,

have

been replaced

and will be examined

by

Engineering.

The inspector will follow-up the results of Engineering's

evaluation of

operational

temperature

data during routine. inspection.

Administrative temperature limit for the containment, if no technical

specification limit exists.

Not Applicable,

see

item 4.

Recent history of temperatures

inside containment.

Provide containment

average air temperature

in addition to the containment air temperatures

to compute the average

containment

temperatures

for the months of April,

May, June, July, August,

and September

1987, if the plant has not

operated

during those

months

use

an operating period close to these

months.

A table was forwarded to

NRR separately

showing the daily containment

average

temperatures,

recorded in accordance

with TS surveillance

requirement 4.6. 1.5, for the months of April to October

1987 for Units

182 and April to October 1988 for Unit 2.

Days where data

was not

recorded

the unit was not in Mode 1 to 4.

Cs