ML16342A752

From kanterella
Jump to navigation Jump to search
Insp Repts 50-275/99-03 & 50-323/99-03 on 990124-0306.Three Violations Noted & Being Treated as Noncited Violations. Major Areas Inspected:Operations,Maint,Engineering & Plant Support
ML16342A752
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 04/05/1999
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML16342A751 List:
References
50-275-99-03, 50-275-99-3, 50-323-99-03, 50-323-99-3, NUDOCS 9904120267
Download: ML16342A752 (52)


See also: IR 05000275/1999003

Text

ENCLOSURE

U.S. NUCLEAR REGULATORYCOMMISSION

REGION IV

Docket Nos.:

License Nos.:

Report No.:

Licensee:

Facility:

Location:

Dates:

Inspectors:

Approved By:

50-275

50-323

DPR-80

DPR-82

50-275/99-03

50-323/99-03

Pacific Gas and Electric Company

Diablo Canyon Nuclear Power Plant, Units 1 and 2

7 ~/~ miles NW of Avila Beach

Avila Beach, California

January 24 through March 6,1999

David L. Proulx, Senior Resident Inspector

Dyle G. Acker, Resident Inspector

David E. Corporandy, Resident Inspector

Linda J. Smith, Chief, Project Branch E

ATTACHMENT: Supplemental Information

'P904i20267 990405

PDR

ADQCK 05000275

8

PDR

I

EXECUTIVE SUMMARY

Diablo Canyon Nuclear Power Plant, Units 1 and 2

NRC Inspection Report No. 50-275/99-03; 50-323/99-03

This inspection evaluated aspects of licensee operations, maintenance,

engineering, and plant

support.

The report covers a 6-week period of resident inspection.

~oerationa

The planning, preparations, and execution of the two draindowns of the Unit 1 reactor to

reduced inventory conditions were generally conducted in a conservative manner.

Licensee contingencies and compensatory actions were appropriate to the

circumstances

(Section 01.2).

. In Mode 6, while pressurizing the primary relief tank with nitrogen during the draindown

to midloop, operators did not have a full understanding of its effect on reactor vessel

level. As a result, reactor vessel level dropped approximately 2 feet in an uncontrolled

manner, and water flowed into the steam generator tubes.

No procedural limits were

exceeded

(Section 01.2).

The first example of a noncited violation of Technical Specification 6.8.1.a. for failure to

properly implement a procedure, involved the draindown to midloop (AR A0479457).

The "Mid Loop Trouble" alarm was not enabled to alert operators of reactor vessel

refueling level high or low, as required (Section 01.2).

With the exception of minor performance and communications problems, which

occurred during performance of the initial steps of refueling, all parties involved in the

fuel load performed well. Performance during core alterations was improved in that

procedure and performance concerns identified in Refueling Outage 2R8 were corrected

for Refueling Outage 1R9 (Section 01.3).

Clearance performance during Refueling Outage 1R9 improved as compared to

previous outages.

A sampling of clearances that the inspectors examined revealed only

one minor error.

In addition, the licensee identified fewer significant clearance errors.

than during Refueling Outage 2R8, indicating that corrective actions have improved

clearance performance (Section 01.4).

Operators failed to revise the risk assessment

of performing the residual heat removal

(RHR) system flush during power operation when they elected to include removal of the

boric acid storage tanks from service.

Operators understood that the boric acid storage

tanks were of low risk significance and, because

of,weak knowledge of the on-line

maintenance

risk assessment

procedure, believed that a revision of the risk assessment

was unnecessary.

Subsequent

evaluation of the risk associated

with this activity

confirmed the risk was low. (Section 04.1).

Operating procedures were not conservative with respect to monitoring spent fuel pool

temperature since increased temperature monitoring was not required with a full core

offload in the spent fuel pool. Operators continued to monitor the Unit 1 spent fuel pool

temperature every 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. As a result, following an inadvertent trip of Spent Fuel

Cooling Pump 1-2, the pump trip went undetected for 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> until a spent fuel pool high

temperature annunciator alarmed (Section M1.3).

Maintenance

The first example of a noncited violation of Technical Specification 6.8.1.a. for failure to

properly preplan maintenance was identified during the initial draindown of the Unit 1

reactor to midloop (AR A0476823).

Isolation of the nitrogen overpressure for the

primary relief tank resulted in reactor vessel level perturbations (Section 01.2).

The second example of a noncited violation of Technical Specification 6.8.1.a. for not

properly preplanning maintenance,

which was associated with replacing a relay that

provided Phase A containment isolation capability (AR A0478430), was identified. The

relay was removed without adequate

precautions or consideration for the effect on plant

equipment.

As a result, the operating spent fuel pool cooling pump tripped from service

without operator knowledge (Section M1.3).

~

A noncited violation of Technical Specification 6.8.1a. for failing to provide a procedure

appropriate to the circumstances

(AR A0479274) was identified. In this instance, the

procedure used to restore the 500 kV offsite power source provided vague guidance for

positioning the main turbine protective trip switches.

In addition, lack of a questioning

attitude on the part of operators restoring the 500 kV power contributed to the trip signal,

partial loss of offsite power, and inadvertent diesel engine generator (DEG) start.

Operator response

in restoring shutdown and spent fuel pool cooling following the loss

of 500 kV power was good (Section M1.4).

~ 'ollowing the failure of DEG 1-1 to reach rated voltage within its acceptance

criteria,

troubleshooting to determine the cause of the problem was generally thorough and

identified a suspect voltage regulator.

Troubleshooting appropriately considered vendor

recommendations

and collected data and the number and frequency of tests exceeded

requirements (Section M1.5).

~En ineerin

~

The prompt operability assessment

associated

with fibrous material in fire stops in

containment in both units, while technically sound, was not timely given the potential

safety significance of inoperable containment recirculation sumps.

The operability

question of the containment recirculation sumps was identified in October 1998.

However, the prompt operability assessment

was not completed until February 1999

The inspectors identified a deficiency in the operability process, specifically, the "issue

needing validation to determine the impact on operability" portion. The licensee had

missed two opportunities to perform a prompt operability assessment

in December 1998

when forced outages had occurred in each unit (Section E1.1).

On January 14, 1998, a violation of 10 CFR 50.59 resulted because the licensee

implemented a design change and failed to submit a license amendment for a change to

the facilitythat involved an unreviewed safety question.

The NRC, however, is

exercising enforcement discretion in accordance with Section VII.B.6 of the enforcement

policy and is refraining from issuing a Notice of Violation. The licensee changed the

configuration of the 230 kV offsite power source from dependence

on Morro Bay for

operability to dependence

on load tap changing transformers and capacitor banks.

Corrective actions for previous 10 CFR 50.59 violations sufficiently addressed

this issue.

The design change improved the reliability of the 230 kV system (Section E1.2).

Plant Su

ort

The second example of a noncited violation of Technical Specification 6.8.1.a for failure

to followprocedure resulted when chemists failed to sample the chemical and volum'e

control system demineralizer prior to placing it in service (NCR N0002084).

This error

resulted in a significant chloride intrusion into the reactor coolant system and caused the

Equipment Control Guideline limit to be exceeded.

In addition, the controls for the

purchase, control, and dedication of resins for nonsafety-related applications were

deficient. The licensee performed a detailed root cause analysis and corrective actions

addressed

the issues appropriately (Section R1.1).

Re ort Details

Summa

of Plant Status

Unit 1 began this inspection period at 100 percent power.

Unit 1 began coasting down for the

end of the fuel cycle on February 3, 1999, and was at 93 percent power on February 7. On

February 7, Unit 1 was shut down to commence Refueling Outage 1R9.

Unit 1 was in Mode 5

(Cold Shutdown) at the end of this inspection period.

Unit 2 operated at essentially 100 percent power during this inspection period.

I. ~Oerations

01

Conduct of Operations

01.1

General Comments

71707

The inspectors visited the control room and toured the plant on a frequent basis when

on site, including periodic backshift inspections.

In general, the performance of plant

operators reflected a focus on safety, evidenced by self- and peer-checking.

Operator

use of three-way communications continued to improve, and operator responses

to

alarms were usually observed to be prompt and appropriate to the circumstances.

01.2

Midloo 0 erations

Unit 1

a.

Ins ection Sco

e 71707

The inspectors observed the licensee's performance related to draining the Unit 1

reactor coolant system to reduced inventory. This inspection included:

(1) review of

training, procedures, and safety assessments,

(2) plant tours, (3) interviews, and (4)

observation of on-shift personnel.

b.

Observations and Findin s

General

During Refueling Outage 1R9, the licensee drained the reactor coolant system to

midloop on two occasions to install and remove reactor coolant loop nozzle dams, which

supported steam generator eddy current inspection.

The midloop operations were

performed with fuel in the reactor vessel.

Most significantly, the steam generator nozzle

dams were installed shortly after the Unit 1 reactor shutdown, when the decay heat load

was high. The inspectors determined that this was a risk significant configuration.

-2-

Plannin

and Pre arations

Technical Specifications required only one DEG, one source of offsite power, and one

RHR pump to be operable with the plant in Mode 5 (cold shutdown).

However, the

licensee determined that additional safety systems would be made available because of

the increased risk when in reduced inventory. Procedures

OP A-2:II "Reactor Vessel-

Draining the Reactor Coolant System to the Vessel Flange - with Fuel in the Vessel,"

Revision 20, and OP A-2:III,"Reactor Vessel - Draining to Half Loop/Half Loop

Operations with Fuel in the Vessel," Revision 20, required many systems in excess of

those required by the Technical Specifications to be available (e.g., two sources of

offsite power, two DEGs, two RHR pumps, and containment closure).

Other

contingencies included stationing operators at the intake structure near the auxiliary

saltwater pumps and in the auxiliary building near the RHR pumps to recover these

important systems,

if necessary.

In addition, the licensee staged a senior reactor operator at the radiological control

access point to screen work to ensure that midloop operations would not be impacted.

The outage safety plan for Refueling Outage 1R9 also required operators to receive

simulator training on reduced inventory operations, including the offsite power sources

to be protected, so work that could impact midloop operations would not be performed.

The inspectors concluded that the planning, preparations, and contingencies showed

'ppropriate sensitivity to effective implementation of refueling activities. On February

10, the inspectors independently verified that these contingencies were satisfactorily in

place prior to commencement of the reactor coolant system draindown.

~Hot Midloo

On February 12, 1999, the licensee commenced the draindown to midloop with a high

decay heat load. During this draindown, the narrow-range reactor vessel refueling level

indication system (RVRLIS) diverged from the wide-range RVRLIS system several times

by more than 4 inches, such that operators had to stop the draindown and direct

technical maintenance personnel to filland vent the RVRLIS detectors.

During one such divergence, operators checked the nitrogen overpressure

of the

primary relief tank. Procedure OP A-2:II required the pressure to be set at 3 psig;

however, operators discovered that the pressure read 0 psig and inspected the nitrogen

supply lineup. Operators determined that the nitrogen supply was inadvertently isolated,

as specified in Clearance 60376, for maintenance unrelated to the midloop operations.

Operators wrote an action request (AR) to enter this item into the corrective action

program.

. Following identification that the nitrogen was isolated, operators quickly cleared the tags

and opened the nitrogen system isolation valves.

Restoring the nitrogen overpressure

to the primary relief tank resulted in a sudden and uncontrolled level drop of 2 feet. The

level decrease

stopped at 111 feet, which was significantly above midloop (107 feet,

~ 8 inches) but was neither controlled nor understood by the operators.

The manager in

charge halted the draindown to midloop until an investigation was completed and the

cause of the level perturbations and sudden drop was understood.

The licensee

-3-

determined that the level dropped because

the nitrogen overpressure

pushed water into

the empty steam generator tubes.

Procedure OP A-2:II, Section 4.4, required operators to review the clearance and

jumper logs to identify any work that could impact reduced inventory operations, prior to

commencing the draindown.

Since this step had been previously signed off as

completed satisfactorily, the inspectors were concerned about the thoroughness

of this

review. The licensee determined that Clearance 60376 had not yet been listed as an

active clearance when operators reviewed the clearance log. Consequently, the

licensee reverified each of the prerequisites, including any clearances that were in the

process of being hung but were not yet active, and recommenced the draindown.

Because Clearance 60376 was initiated without reviewing its impact on RVRLIS and

midloop operations, this maintenance activity was not properly reviewed for the

circumstances.

This licensee-identified deficiency is the first example of a violation of

Technical Specifications 6.8.1.a for failure to properly preplan maintenance.

However,

this Severity Level IVviolation is being treated as a noncited violation, consistent with

Appendix C of the Enforcement Policy. This violation is in the corrective action program

as AR A0476823 (50-275/99003-01).

Following resolution of the RVRLIS issues, the licensee completed the draindown. The

inspectors noted that the rest of the evolution, including installation of nozzle dams and

refill of the reactor coolant loops, was completed satisfactorily and in a conservative

manner.

Second Midloo

On March 4, operators commenced a second draindown to midloop to remove the

steam generator nozzle dams.

The licensee instituted similar contingencies and

preparations as with the hot midloop. Decay heat load was significantly less than the

earlier midloop condition in that one-third of the fuel had not been irradiated following

core reload and the reactor had been shut down for approximately

1 month. Therefore,

engineers determined that the second draindown to midloop had less risk significance

than the first. The inspectors verified that a sampling of the prerequisites had been

satisfactorily completed.

During the draindown, with RVRLIS level stabilized at 109 feet, the inspectors

questioned whether operators had enabled the "Mid Loop Trouble" alarm.

Procedure OP A-2:III,step 6.1.1, required the operators to verify that the narrow range

RVRLIS level alarms had been enabled.

Operators had previously enabled both the

"RVRLIS High/Low"and the "Mid Loop Trouble" alarms.

These annunciators provided

operators with warnings to prevent RVRLIS level from being too high such that it would

impact personnel remo'ving nozzle dams or too low such that vortexing of the reactor

water inventory could impact the operating RHR system.

However, prior to

commencement of draindown, operators inadvertently disabled the "Mid Loop Trouble"

alarm by setting up operating bands using the plant process computer select function.

-4-

Procedure OP A-2:III,Section 4.5.1, permitted operators to establish operating bands

using the plant process computer select function in addition to enabling the

normal-range RVRLIS level alarms.

Operators were not aware that using the plant

process computer select function could effect the narrow-range RVRLIS system.

Upon the inspectors'uestioning,

operators determined that Procedure OP A-2:III,Step

6.1.1, had not been fullyimplemented.

The shift foreman initiated AR A0479457 to

enter this item into the corrective action system, and the control operator restored the

"Mid Loop Trouble" alarm to operation.

The draindown and refill of the reactor coolant

loops was completed without further incident. The failure to enable the "Mid Loop

Tr'ouble" alarm prior to draindown is the first example of a violation of Technical Specification 6.8.1.a for failure to followprocedure.

However, this Severity Level IV

violation is being treated as a noncited violation, consistent with Appendix C of the

Enforcement Policy. This violation is in the corrective action program as AR A0479457

(50-275/99003-02).

Conclusions

The planning, preparations, and execution of the two draindowns of the Unit 1 reactor

coolant system to midloop were generally conducted in a conservative manner.

Licensee contingencies and compensatory actions were appropriate to the

circumstances.

The first example of a noncited violation of Technical Specification 6.8.1.a. for failure to

properly preplan maintenance was identified during the initial draindown of the Unit 1

reactor to midloop (AR A0476823).

Isolation of the nitrogen overpressure for the

primary relief tank resulted in reactor vessel level perturbations.

In Mode 6, while

pressurizing the primary relief tank with nitrogen during the draindown to midloop,

operators did not have a full understanding of its effect on reactor vessel level. As a

result, reactor vessel level dropped approximately 2 feet in an uncontrolled manner, and

water flowed into the steam generator tubes.

No procedural limits were exceeded.

The first example of a noncited violation of Technical Specification 6.8.1.a. for failure to

properly implement a procedure, involved the draindown to midloop (AR A0479457).

The "Mid Loop Trouble" alarm was not enabled to alert operators of reactor vessel

refueling level high or low, as required.

Refuelin

Activities

Ins ection Sco

e 71707

On February 27, 1999, the inspectors observed refueling activities in the control room,

fuel building, and containment.

These activities included handling and movement of the

fuel assemblies from the spent fuel pool to the upender and from the upender to the

final core location, control room monitoring of required parameters,

reactor engineering

calculations of inverse count rate ratio, and monitoring of fuel location for accountability

-5-

requirements.

The inspectors reviewed Procedures

OP B-8DS2, "Core Loading,"

Revision 21, and PEP R-8DS2, "Core Loading Sequence,"

Revision 1, which contained

the procedure requirements for these activities.

Observations and Findin s

Ultrasonic inspection of the reactor pressure vessel outlet nozzles was required to be

complete prior to beginning fuel load. Ultrasonic inspection of the reactor pressure

vessel nozzles was completed several hours ahead of time, which created an

opportunity to begin fuel load earlier than scheduled.

Lighting, tools, and other

equipment and prerequisites for fuel load had not been prestaged.

Consequently, the

opportunity to start fuel load ahead of time passed.

Communication of status, duration,

and level of effort to complete these activities was, at times, not clearly communicated.

The operations shift foreman appropriately delayed the start of fuel load until

prerequisite items were verified to be complete.

Senior managers were promptly

informed of the communication problem and intervened in a timely manner to alleviate

the problem.

During performance of the initial steps of Procedure PEP R-8DS2, Fuel Assembly AA83

was raised out of the spent fuel pool rack prior to unloading Fuel Assembly BB04 from

the upender inside of the containment, which was contrary to management

expectations.

The control room operators immediately recognized this and informed the

shift foreman.

The shift foreman briefly suspended

further core load to make sure that

the involved parties understood the management expectations.

The inspectors

observed a significant portion of the fuel load activities. Other'than the minor

performance issue described above, the fuel load activities observed by the inspectors

were accurately performed in a deliberate manor.

During the last Unit 2 refueling outage, a violation was identified for failing to restore the

source range detector high flux at shutdown alarm, as instructed in the core load

procedures.

Complex instructions and failing to clearly specify the person responsible

for completing the actions were identified as contributing causes.

For this Unit 1

refueling outage, each action was clearly defined in the procedure, and a specific

individual was assigned responsibility for completing the actions.

The core loading

procedures required that criticality be calculated after the first 13 fuel assemblies are

loaded next to their applicable detector and for each fuel assembly added thereafter.

Procedure OP B-'8DS2, step 5.7.7, states "Criticalityis indicated when the inverse count

rate ratio approaches

zero, and if the straight line determined by the last two Inverse

count rate ratios for a ~res ondin

detector indicates that criticality could occur if the next

twelve (12) or less fuel assemblies

are loaded." The inspectors observed the reactor

engineers verify source range detector count rates and calculate the inverse count rate

ratio. Work was satisfactorily accomplished

in a timely manner to support fuel load

activities.

The inspectors observed the refueling senior reactor operator directing the fuel handling

operations in containment.

The refueling senior reactor operator maintained good

supervision over the activities, maintained communications with the control room and

4

M

-6-

the personnel in the fuel building, provided clear directions to the crane operator and

other observers, verified the correct core location using the fuel movement tracking

sheets, monitored the load on the manipulator crane, and confirmed the proper

indicating lights and Z-Z tape position.

The inspectors also observed that the foreign material exclusion area controls around

the reactor cavity and the spent fuel pool were effective.

Conclusions

With the exception of minor performance and communications problems, which

occurred during performance of the initial steps of refueling, all parties involved in the

fuel load performed generally well. Performance during core alterations was improved,

in that procedure and performance concerns identified in Refueling Outage 2R8 were

corrected for Refueling Outage 1R9.

01.4

Clearance Performance

a.

Ins ection Sco

e 71707

92901

During Unit 2 Refueling Outage 2R8, operators committed a number of significant

clearance errors.

These errors were discussed

in NRC Inspection Report

50-275; 323/98-07, and a violation was issued for several examples of failing to properly

implement the clearance procedure.

Because of this deficient performance, the

inspectors evaluated the clearance order implementation during Refueling Outage 1R9

to determine the effectiveness of'the previous corrective actions.

The evaluation

included walkdowns of several clearances

and reviews of licensee-identified issues.

b.

Observations and Findin s

The inspectors walked down several clearance orders.

Of these clearances,

the

inspectors identified one minor error. On February 12, 1999, the inspectors identified

that tags hung for maintenance on breakers associated with the control rod drive motor

generator sets were man-on-line tags while the clearance called for caution tags.

The

breakers were in the correct position, and the tags were hung on the correct

components; therefore, personnel and equipment safety were not jeopardized.

Personnel initiated an event trend record to document this occurrence, and the

operations director issued a shift order to remind operators to verify that the proper type

.

of tag was hanging, as well as the correct component and position. The inspectors

noted that the clearances walked down were otherwise satisfactory.

In addition, the inspectors reviewed clearance issues identified on nine ARs. One

AR Addressed a man-on-line tag hung on the wrong switch. A second AR discussed

an

issue that involved several tags being removed with work in progress.

The rest of the

ARs discussed administrative violations of procedures.

In comparison, during Refueling

Outage 2R8, the licensee committed eight errors that the inspectors considered

significant; each incident involved a lack of tagging protection while work was in

progress.

The licensee initiated numerous corrective actions as docketed in the

0

-7-

response to NRC Inspection Report 50-275; 323/98-07.

The inspectors concluded that,

although the licensee achieved significant improvement in performance of clearances

because

of these corrective actions, further improvement in this area is still necessary.

C.

Conclusions

Clearance performance during Refueling Outage 1R9 improved as compared to

previous outages.

A sampling of clearances that the inspectors examined revealed only

one minor error.

In addition, the licensee identified fewer significant clearance errors

than during Refueling Outage 2R8, indicating that corrective actions have improved

clearance performance.

04

Operator Knowledge and Performance

04.1

RHR S stem Flush

Ins ection Sco

e 71707

The inspectors witnessed the flush of the RHR system, including the probablistic risk

assessment

to support the evolution.

Observations and Findin s

On February 3, 1999, operators performed a flush of the Unit 1 RHR system in

preparation for plant cooldown during upcoming Refueling Outage 1R9. The licensee

previously performed this evolution following plant shutdown so that when RHR was

initiated, the chemistry of the reactor coolant system would not be adversely affected.

Prior to the flush, the probablistic safety assessment

group evaluated the evolution with

respect to risk. The RHR system flush required isolation of the RHR system, which

rendered the system inoperable for the low pressure safety injection mode of operation

and required entry into a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> shutdown action statement for approximately 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />

total for each train. The engineers noted that removing each RHR train from service to

support the flush was not risk significant when evaluated using industry guidelines.

The

shift foreman reviewed and approved this safety assessment

prior to commencement

of

the RHR system flush.

In preparation for the flush, operators reviewed Procedure OP B-2:V, "RHR - Place in

Service During Plant Cooldown," Revision 17, and noted that the procedure required

several flow paths to be established simultaneously.

Procedure OP B-2:V directed the

user to flush water from the RHR system by draining to the radwaste system while filling

from the refueling water storage tank. To maintain refueling water storage tank levels,

the procedure required the transfer of water from the boric acid storage tanks.

In

addition, boric acid storage tank inventory would be maintained via the makeup system.

Operators determined that control of the evolution would be optimized if fewer flow

paths were in service simultaneously.

Therefore, the shift foreman determined that

boric acid storage tank levels would not be maintained while the evolution was in

0

-8-

progress.

The boric acid storage tanks would be refilled once the evolution was

completed.

Performing Procedure OP B-2:V in this alternative manner required

operators to declare the boric acid storage tanks inoperable and enter a 72-hour

shutdown action statement.

At the start of the RHR system flush, operators performed a briefing and entered the

applicable limiting conditions for operation.

Following commencement

of the RHR

system flush, the inspectors reviewed the approved probablistic safety assessment.

The inspectors noted that the probablistic safety assessment

included the RHR system

.

as unavailable but did not recognize the inoperability of the boric acid storage tanks.

The shift foreman stated that the boric acid storage tanks were not risk significant and

need not be evaluated.

The shift foreman noted that Procedure AD7.DC6, "On-Line

Maintenance Risk Assessment,"

Revision 2, contained a matrix of the risk significant

s'ystems and that the boric acid storage tanks were not included in this matrix.

In

addition, the boric acid storage tanks were not modeled in the on-line computer program

for risk assessment.

However, the inspectors noted that Procedure AD7.DC6, Section 6.5, required a

two-step approach to on-line risk assessment.

The first step was a probablistic safety

assessment

using the plant computer and the matrix.

In addition, Procedure AD7.DC6,

Attachment 9.5, required a deterministic approach to assess

safety significance.

This

section was based on defense-in-depth

of the critical safety functions referenced

in the

emergency operating procedures.

Procedure AD7.DC6, Section 6.5, was developed to

ensure operators did not cause an inadvertent total loss of safety function and violate

the Technical Specifications by removing multiple nonrisk significant systems from

service.

The inspectors discussed the deterministic assessment

required by

Procedure AD7.DC6 with the operating crew and identified that the crew was not

cognizant of this element of safety assessment.

Operators then performed the

deterministic review and determined that the configuration of having one RHR pump

inoperable coincident with the boric acid storage tanks being inoperable was allowed by

procedure and was nonrisk significant.

The inspectors discussed this issue with the Operations Director. The Operations

Director evaluated the operator knowledge of Procedure AD7.DC6 and identified that

most of the other operating crews were similarly unfamiliar with the two-step approach

to risk assessment.

The operations department conducted "just-in-time" training on the

specifics of Procedure AD7.DC6 for each of the operating crews. The inspectors

concluded that this training sufficiently addressed

the concern with the RHR flush and

the lack of revision of the risk assessment.

Conclusions

Operators failed to revise the risk assessment

of performing the RHR system flush

during power operation when they elected to include removal of the boric acid storage

tanks fro'm service.

Operators understood that the boric acid storage tanks were of low

risk significance and, because

of weak knowledge of the on-line maintenance

risk

assessment

procedure, believed that a revision of the risk assessment

was

unnecessary.

Subsequent

evaluation of the risk associated

with this activity confirmed

the risk was low.

e

M1

Conduct of Maintenance

M1.1

Maintenance Observations

a.

Ins ection Sco

e 62707

The inspectors observed all or portions of the following work activities:

Work Order R0170936, Component Cooling Water Heat Exchanger 1-2, clean

and inspect seawater side

Install steam generator nozzle dams to support eddy current testing.

b.

Observations and Findin s

The inspectors concluded that each of these work activities was performed satisfactorily.

M1.2

Surveillance Observations

Ins ection Sco

e 61726

Selected surveillance tests required to be performed by the Technical Specifications

were reviewed on a sampling basis to verify that:

(1) the surveillances were correctly

included on the facilityschedule; (2) technically adequate procedures existed for the

performance of the surveillances; (3) the surveillances had been performed at a

frequency specified in the Technical Specifications; and (4) test results satisfied

acceptance

criteria or were properly dispositioned.

The inspectors observed all or portions of the following surveillances:

STP M-81A

Diesel Engine Generator Inspection (Every Refueling Outage),

Revision 13

STP M-9L

Diesel Generator Shutdown Lockout Relay Test, Revision 21

STP M-86G

NUREG 0737: Charging System (Suction) Leak Reduction and

Leak Check of Charging Pumps Suction, Revision 16

b.

~

Observations and Findin s

The inspectors concluded that each of these surveillance activities was performed

satisfactorily.

0

M1.3

Loss of S ent Fuel Pool Coolin

-10-

Ins ection Sco

e 62707 92902

The inspectors evaluated the licensee response

to AR A0478430 and Quality

Evaluation Q0012110,, which identified an inadvertent loss of spent fuel pool cooling.

Observations and Findin s

On February 25, 1999, at 5:06 p.m., operators received the Unit 1 "Spent Fuel Pool

Level/Temp" annunciator in the control room. Upon checking the plant computer,

operators recognized that the alarm resulted from an elevated temperature of 125 F in

the spent fuel pool. The shift foreman dispatched a nuclear operator who noted that the

local temperature gauge for the spent fuel pool indicated 126'F. The nuclear operator

found that Spent Fuel Pool Pump 1-2 was not operating as required and rest'arted the

pump. Since the cause of the trip was unknown at this time, the shift foreman directed

hourly checks of Spent Fuel Pool Pump 1-2 to ensure continued operation.

Following

restart of the pump, spent fuel pool temperature gradually returned to the normal

temperature of 100 F.

The licensee determined from operator logs taken on February 25 that Spent Fuel Pool

Pump 1-2 was running at approximately 11 a.m, with a spent fuel pool temperature of

100'F.

Upon search of plant records, the licensee determined that Relay CIAX-H

(associated with the Containment Phase A isolation signal) had been replaced that day.

One of the purposes of the control circuit for Relay CIAX-His to trip the spent fuel pool

cooling pumps during an accident to prevent overloading of the DEGs. Since

Relay CIAX-Hhad been removed at approximately

1 p.m., the licensee concluded that

spent fuel pool cooling had been lost for 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />.

Engineers determined that the heatup

rate was approximately 6'F per hour and that the time to boil the spent fuel pool was

approximately 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br />.

Upon review of Work Order 60444, the inspectors noted that the clearance associated

with the procedure contained no precautions or limitations to notify operators of th'e trip

of the spent fuel pool cooling pump when removing Relay CIAX-H. Had this precaution

.been in place, operators could have immediately restarted Spent Fuel Pool Pump 1-2,

preventing the inadvertent heatup of the spent fuel pool. Because this precaution was

not in the clearance associated with Work Order 60444, this maintenance activity was

not appropriately preplanned for the circumstances.

The failure to properly preplan the

replacement of Relay CIAX-His the second example of a violation of Technical Specifications 6.8.1.a.

However, this Severity Level IVviolation is being treated as a

noncited violation, consistent with Appendix C of the Enforcement Policy. This violation

is in the corrective action program as AR A0478430 and Quality Evaluation Q0012110

(50-275/99003-01).

The inspectors noted that a contributing cause to the event was the inadequate

monitoring of the spent fuel pool. As of February 18, the Unit 1 core was fullyoffloaded,

which significantly increased the heat load of the spent fuel pool. No control room

indications or controls of spent fuel pool pumps or spent fuel pool temperature/level

existed at Diablo Canyon.

However, operators continued to check spent fuel pool

-11-

parameters

every 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />, even though the heat load in the spent fuel pool had

increased.

The inspectors concluded that, with monitoring every 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />, margin

existed for operators to take action prior to boiling in the spent fuel pool, since the time

to boil was 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br />.

In addition, with the spent fuel pool temperature alarm set at

125'F, operators had sufficient time to restore spent fuel pool cooling prior to fuel pool

temperature exceeding the design basis limitof 140 F. However, the inspectors

concluded that failing to frequently monito'r spent fuel pool temperature following a full

core off-load was an example of nonconservative operation.

Following the loss of spent fuel cooling event of February 25, the licensee revised

Procedure B-8DS1, "Core Unloading," Revision 21, to require checks of the operating

spent fuel pump and spent fuel pool temperature every 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> while the core was

offloaded.

The inspectors concluded that this procedure change was appropriate.

Conclusions

The second example of a noncited violation of Technical Specification 6.8.1.a. for not

properly preplanning maintenance,

which was associated

with replacing a relay that

provided Phase A containment isolation capability (AR A0478430), was identified. The

relay was removed without adequate precautions or consideration for the effect on plant

equipment.

As a result, the operating spent fuel pool cooling pump tripped from service

without operator knowledge.

Operating procedures were not conservative with respect to monitoring spent fuel pool

temperature since increased temperature monitoring was not required with a full core

offload in the spent fuel pool. Operators continued to monitor the Unit 1 spent fuel pool

temperature every 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. As a result, following an inadvertent trip of Spent Fuel

Cooling Pump 1-2, the pump trip went undetected for 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />, until a spent fuel pool

high temperature annunciator alarmed.

Unit 1 Loss of 500 kV and DEG Start

Ins ection Sco

e 61726 92902

t

The inspectors evaluated the licensee response to a Unit 1 turbine trip signal that

occurred on March 3, 1999, while the unit was in Mode 6.

Observations and Findin s

On March 3, while Unit 1 was in Mode 6, in parallel with the preparations being made to

test the Bus G auto transfer to DEG 1-2, the main turbine oil and condensate

systems

were being returned to service.

At approximately 3 p.m., a turbine trip signal caused the

auto-transfer of the Unit 1 electrical buses from the 500 kV offsite auxiliary power source

to the 230 kV offsite startup power source.

Vital Bus G did not transfer because

its

startup feeder breaker was in the "Test" position in preparation for DEG 1-2 surveillance

testing, as specified in Procedure M-13G, "4 kV Bus G Non-Sl Auto-Transfer Test,"

Revision 16A. DEG 1-2 automatically started and the bus loads stripped, as designed

for a loss of offsite power. As a consequence,

RHR Pump 1-1 tripped (pump providing

shutdown cooling), as well as Spent Fuel Pool Pump 1-2. The loads did not sequence

-12-

onto Bus G because

no safety injection signal was present.

Operators responded

promptly to restart RHR Pump 1-1 within 39 seconds and Spent Fuel Pool Pump 1-2

within approximately 5 minutes. After stabilizing the plant, the operators paralleled

DEG 1-2 to startup power, then unloaded, separated,

and secured DEG 1-2.

Prior to restoring the 500 kV auxiliary power to Unit 1, Operations investigated the event

to gain a basic understanding of its cause.

At the beginning of the refueling outage on

February 7, Unit 1 electrical buses were transferred to the 230 kV startup power, and

the unit was separated from the grid. Subsequently, auxiliary power was restored for

backfeeding in accordance with Procedure OP J-2:V, "Backfeeding the Unit from the

500 kV System," Revision 3B, and electrical buses were transferred back to the 500 kV

auxiliary power., Part of Procedure OP J-2V applies administrative tagouts to disable

turbine protection related trips that could open the 500 kV generator output breakers.

At

this time, operators properly disabled turbine thrust bearing wear trip along with other

turbine trips.

On February 13, electrical buses were'transferred

to startup power, and the 500kV

transformer banks were cleared for outage-related

maintenance.

On February 25,

maintenance was completed, and operators were assigned to restore the 500 kV

auxiliary power.

During the restoration, operators used Procedure OP J-2:I, "Main'and

Aux Transformer Return to Service," Revision 9, to restore the 500 kV power.

Procedure OP J-2I specifically directs placing the transformer protection switches in

service but is vague about positioning the other turbine trip protection switches.

In the

absence of specific guidance, the operators erroneously placed the thrust bearing wear

trip in service.

The failure to properly implement procedures for restoring the 500 kV

electrical power is a violation of Technical Specification 6.8.1a because of its impact on

safety-related equipment.

This Severity Level IVviolation is being treated as a noncited

violation, consistent with Appendix C of the NRC Enforcement Policy. This violation is in

the corrective action program as AR A0479274 and Nonconformance Report N0002089

(50-275/99003-03).

Also, the licensee investigated the cause of the high thrust bearing wear trip. Various

turbine and generator related oil pumps were being restored and tested throughout the

day. Because the main turbine thrust bearing trip nozzle assembly had not yet been

aligned, the thrust bearing was in a position that caused the trip oil pressure to rise

above its trip setpoint when the auto-.stop oil system was pressurized by the pump

starts.

After understanding the basic steps that led to the Unit 1 trip, on-the-spot

procedure changes were made to incorporate the specific instructions outlined in

Procedure OP J-2:V to disable turbine protection related trips that could potentially open

the 500 kV breakers.

Operators used the revised procedures to restore 500 kV power.

Approximately 3~/~ hours elapsed from the time of loss of 500 kV auxiliary power until its

restoration.

The inspectors agreed with the assessment

that procedure deficiencies led to the

misalignment of the thrust bearing trip switch and contributed to the turbine trip.

However, the inspectors concluded that the operators who performed the procedure

should have clarified the unclear procedure guidance before positioning trip circuits.

Operations personnel subsequently reviewed similar electrical restoration procedures,

and several changes were made to clarify vague guidance on positioning trip circuits.

0

-13-

Also, the licensee identified a weakness

in the sequence

of steps for performing the

auto-transfer test.

Procedure M-13G requires that the Bus G startup feeder breaker be

racked into the "Test" prior to simulating the loss of 500 kV auxiliary power. Subsequent

steps in the procedure instruct the operators to start RHR Pump 1-2, which is powered

by Bus H, since the Bus G RHR pump willbe stripped off the bus and not automatically

restarted.

Operators concluded that Procedure M-13G could be improved by placing

the step to start the other RHR pump prior to the step to rack the Bus G startup feeder

breaker into the "Test" position.

Conclusions

A noncited violation of Technical Specification 6.8.1a. for failing to provide a procedure

appropriate to the circumstances

(AR A0479274) was identified. In this instance, the

procedure used to restore the 500 kV offsite power source, in this instance, provided

vague guidance for positioning the main turbine protective trip switches.

In addition,

lack of a questioning attitude on the part of operators restoring the 500 kV power

contributed to the trip signal, partial loss of offsite power, and inadvertent DEG start.

Operator response

in restoring shutdown and spent fuel pool cooling following the loss

of 500 kV power was good.

Failure of DEG 1-1 to Pass Time-to-Rated Volta e Test

Ins ection Sco

e 61726

The inspectors evaluated the response to Quality Evaluation Q0012109 and associated

AR A0478728, which described the failure of DEG 1-1 to reach rated voltage within the

13-second acceptance

criteria limitduring a performance test.

Observations and Findin s

During a timed start of DEG 1-1 on February 27, 1999, the DEG took 20.4 seconds to

reach 4160 volts. This exceeded the test acceptance

criteria of 13 seconds and was

considered to be a valid Maintenance Rule functional failure of DEG 1-1. During the

timed start, engineers observed that voltage increased to approximately 2000 volts,

hesitated for approximately 6 seconds, then rapidly rose to the required 4160 volts.

During a normal DEG start, excitation voltage is initiallysupplied to the motor generator

windings until a point of approximately 2700 volts. At approximately 2700 volts, the K3

relay opens to allow the voltage regulator to control the voltage increase to 4160 volts.

Below 2700 volts, the voltage regulator is inefficient. Without the aid of the excitation

voltage, the DEG would be unable to reach its rated 4160 volts within the required 13

seconds.

The engineers conducting the test remembered that a similar problem had occurred in

August/September

1998 and that part of the corrective action involved replacing the K3

relay. Consequently, the engineers decided to replace the K3 relay before resumption

of testing.

The engineers who decided to replace the K3 relay did not realize at this time

that DEG 1-1 was the same DEG that had the K3 relay replaced in September 1998.

-'14-

Prior to retesting DEG 1-1, engineers reviewed a troubleshooting guide provided by

Besler Electric, the manufacturer of the exciter and the voltage regulator.

In order to

gather more information to monitor symptoms, two Windowgraf recorders were installed

to monitor generator output v'oltage, DC field voltage and current, relay actuation

voltage, and transformer current. The inspectors considered the use of the additional

test monitoring equipment to be a prudent measure but opined that the licensee had

missed an additional opportunity to diagnose the problem by replacing the K3 relay prior

to resumption of testing. The licensee bench tested the removed K3 relay and

determined that the K3 relay behaved normally during its bench tests.

Following installation of the Windowgraf recorders, from February 28 through March 4,

five tests were performed with no additional failures.

DEG 1-2 was monitored to obtain

the same test data as for DEG 1-1 as a benchmark.

Test data for the five DEG 1-1

tests and the DEG 1-2 test were similar; consequently, the licensee considered DEG 1-1

to be operable.

Since the additional test data was not sufficient to measure all of the

voltage regulator control card parameters,

the licensee replaced the voltage regulator

control card.

Seven successful tests were performed subsequent

to the voltage

regulator card replacement.

Because of the failures on DEG 1-1 in August 1998 and February 1999, DEG 1-1 was

being tested weekly in accordance with Technical Specification requirements.

As of the

end of the inspection period, the licensee had only two more Technical Specifications

tests to be conducted on the accelerated frequency of once per week versus monthly.

However, the troubleshooting plan recommended that the accelerated

testing be

continued for an additional ten instrumented tests beyond that required by the Technical

Specifications.

Conclusions

Following the failure of DEG 1-1 to reach rated voltage within its acceptance

criteria,

troubleshooting to determine the cause of the problem was generally thorough and

identified a suspect voltage regulator.

Troubleshooting appropriately considered vendor

recommendations,

and collected data and the number and frequency of tests exceeded

requirements.

M8

Miscellaneous Maintenance Issues (92700)

M8.1

Closed

Violation 50-275/97003-04:

failure to take adequate corrective actions to

correct deficiencies in the painting program.

This violation was issued as a result of an improperly painted governor valve linkage on

Turbine-Driven AuxiliaryFeedwater Pump 1-1. On February 28, 1997, the licensee

declared Turbine-Driven Auxiliary Feedwater Pump 1-1 inoperable because

the paint on

the governor valve linkage could potentially impair its movement.

Subsequently,

the

licensee issued Licensee Event Report 50-275/97-004-01

to describe this event.

-15-

The issues discussed

in the licensee event report were discussed

in NRC Inspection

Report 50-275; 323/97-03 and in the violation response letter dated June 18, 1997. The

inspectors verified the corrective actions described in the violation response letter and

licensee event report to be reasonable

and complete.

Closed

Licensee Event Re ort50-275/97-004-01:

Technical Specification 3.7.1.2not

met because of paint applied to auxiliary feedwater pump turbine governor linkage

because

of personal error.

Closure of this followup item is discussed

in Section M8.1.

Conduct of Engineering

Fibrous Material in Containment

Ins ection Sco

e 37551

The inspectors evaluated the corrective actions related to AR A0477669, which

discussed the potential for fibrous material in containment to impact the operability of

the containment recirculation sumps.

Observations and Findin s

On October 22, 1998, upon review of an operating experience report from another

facility, the licensee identified the potential for fibrous material in fire stops of vertical

cable trays to impact containment recirculation sump operability. The engineers were

concerned that this fibrous material could be transported to the containment

recirculation sumps, clog the sumps, and cavitate the operating RHR pumps during the

recirculation phase of a design basis accident.

The licensee initiated AR A0477669 to

enter this item into the corrective action program.

As-built drawings did not have sufficient detail to identify the exact location or quantity of

this fibrous material.

Based on discussions with personnel that performed repairs on fire

stops, the licensee surmised that vertical cable tray fire stops consisted of fibrous

materials known as Kaowool or Marinite. Because of the lack of sufficient detail,

engineers could not initiallydetermine if the fibrous material was installed in

jet-impingement zones or subject to the effects of high energy line breaks.

Based on

the unknown status of the fibrous material, engineers coded this AR As an "issue

needing validation to determine the impact on operability" and did not perform a prompt

operability assessment.

The prompt operability assessment

was scheduled for

performance during Refueling Outage 1R9 in February 1999.

On February 20, 1999, during Refueling Outage 1R9, the licensee inspected the Unit 1

containment to determine the exact location and quantity of fibrous material. The

licensee evaluated or removed the fibrous material the Unit 1 containment located in jet

impingement zones.

The inspectors reviewed the licensee action with respect to Unit 1

and concluded that the action was satisfactory.

On February 20,'he licensee performed a prompt operability assessment

for Unit 2.

Although the licensee did not inspect Unit 2, the licensee noted that both units were

reasonably similar. Ten specific postulated pipe break locations on Unit 1 had

significant fibrous material that could potentially be released

in a jet-impingement zone.

Engineers evaluated the operability of the Unit 2 containment recirculation sumps based

on the Unit 1 information, using accepted transport phenomena calculations.

The

engineers determined that, although the net positive suction head of the RHR pumps

was decreased,

adequate

margin for operability existed.

The inspectors reviewed the

Unit 2 operability assessment

and determined it was satisfactory.

Although the inspectors concurred with the technical merit of the containment

recirculation sump operability assessments,

the inspectors questioned the timeliness of

these evaluations.

The inspectors noted that the operability of the sumps directly

impacted safety and was considered risk significant. Generic Letter 91-18, "Resolution

of Degraded and Nonconforming Conditions and Operability," stated that the timeliness

of operability issues should be commensurate

with the safety significance.

However,

the licensee had two missed opportunities to inspect the containment structures for

fibrous material.

Both Units 1 and 2 sustained forced outages in December 1998, yet

licensee management deferred resolution of this issue until Refueling Outage 1R9.

Conclusions

The prompt operability assessment

associated with fibrous material in fire stops in

containment in both units, while technically sound, was not timely, given the potential

safety significance of inoperable containment recirculation sumps.

The operability

question of the containment recirculation sumps was identified in October 1998.

However, the prompt operability assessment

was not completed until February 1999.

The inspectors identified a deficiency in the operability process, specifically, the "issue

needing validation to determine the impact on operability" portion. The licensee had

missed two opportunities to perform a prompt operability assessment

in December 1998

when forced outages had occurred in each unit.

Modifications to the 230kV Offsite Power S stem

Ins ection Sco

e

The inspectors reviewed the modifications to the offsite power system to address

equipment reliabilityconsiderations and the divestiture of the Morro Bay Power Plant

(Morro Bay) by Pacific Gas and Electric.

Observations and Findin s

The 230 kV offsite power system at Diablo Canyon and the capabilities and

configuration of Morro Bay were described in detail in the Final Safety Analysis Report,

Section 8.2, "Offsite Power System," Revision 11, dated November 1996. The Final

Safety Analysis Report described various configurations of Morro Bay and the effect of

such configurations on the reliability of offsite power at the site. Additionally, the Final

Safety Analysis Report provided information and references to plant procedures that

addressed

contingency actions.

These contingency actions would need to be

-17-

accomplished at Diablo Canyon in the event of equipment failures or outages at Morro

Bay in order to ensure adequate voltage for safety-related equipment.

In late 1997, the licensee began proceeding with modifications that would eliminate the

dependence

of the Diablo Canyon units on Morro Bay. These modifications replaced

the existing startup transformers with load tap changing transformers and added shunt

capacitors to eliminate the need for Morro Bay. These modifications resulted, in part,

from the uncertainty associated with the economic viabilityof Morro Bay in a

deregulated electrical environment that began in January 1998.

In mid-February 1998,

the licensee completed all of the planned modifications associated

with the 230 kV

offsite power system and subsequently divested itself of Morro Bay.

Allof the changes to the facilityand the divestiture of Morro Bay were conducted without

prior approval by the NRC. The screening evaluations conducted by the licensee for the

modifications concluded that the modifications to the offsite power system and the

divestiture of Morro Bay did not constitute an unreviewed safety question and, therefore,

did not require prior NRC approval.

However, based on the questions raised by agency

inspectors, the licensee initiated a management

meeting with the NRC on December 22,

1997, and described the changes that had been made.

As a result of the issues raised

at that meeting, the licensee submitted a license amendment request to the NRC

(Pacific Gas and Electric Letter DCL 98-008, dated January 14, 1998) seeking approval

for the changes that had been implemented.

The license amendment request described

the modifications to the offsite power system and the elimination of the dependence

of

the facilityon Morro Bay. In the submittal, the licensee asserted that the new

configuration represented

a safety improvement at the facilityon the basis of the

assumed superior reliability characteristics of the new equipment.

The inspectors noted that 10 CFR 50.59 states, in part, that a proposed change, test, or

experiment shall be deemed to involve an unreviewed safety question if the possibility of

an accident or malfunction of a different type than any evaluated previously in the safety

analysis may be created.

Further, the inspectors determined that the addition of the

load tap changing transformers along with the shunt capacitors in lieu of the

dependence

on Morro Bay constituted a change to the facilityas described in the Final

Safety Analysis Report and that this change introduced the possibility of a malfunction of

a different type than had been previously analyzed (e.g., the load tap changers may fail

to adjust as required for changes

in voltage or passive failure of the shunt capacitors).

Thus, the inspectors determined that the

10 CFR 50.59 evaluation was inadequate and

that these changes had resulted in an unreviewed safety question.

After consultation with the Director, Office of Enforcement, the NRC is exercising

enforcement discretion in accordance with VII.B.6 of the Enforcement Policy and

refraining from issuing a Notice of Violation. Discretion is appropriate because

of:

(1) confusion surrounding the determination of whether the change constituted an

unreviewed safety question, (2) the similarity to other issues previously cited for which

corrective actions have been taken and are sufficiently broad to address this violation

(EA 98-364), and (3) the apparent improvement in grid reliability that resulted from the

change (50-275; 323/99003-04).

-18-

c

Conclusions

On January,

14, 1998, a violation of 10 CFR 50.59 resulted because the licensee

implemented a design change and failed to submit a license amendment for a change to

the facilitythat involved an unreviewed safety question.

The NRC, however, is

exercising enforcement discretion in accordance with Section VII.B.6of the enforcement

policy and is refraining from issuing a Notice of Violation. The licensee changed the

configuration of the 230 kV offsite power source from dependence

on Morro Bay for

operability to dependence

on load tap changing transformers and capacitor banks.

Corrective actions for previous 10 CFR 50.59 violations sufficiently addressed

this issue.

The design change improved the reliability of the 230 kV system.

ES

Miscellaneous Engineering Issues (92700, 92903)

E8.1

Closed

Licensee Event Re ort 50-275/95-013-02 and -01: component cooling water

system may have operated outside of its design basis

Because of the limited capacity of the auxiliary saltwater system combined with

increases

in the calculated heat load to the component cooling water system, the

component cooling water system may have operated outside of its design basis.

This

issue was discussed

in NRC Inspection Report 50-275; 323/98-05.

No new issues were

revealed by the licensee event report.

V.~

R1

Radiological Protection and Chemistry Controls

R1.1

Reactor Coolant S stem Chloride Intrusion

a.

Ins ection Sco

e 71750 92904

The inspectors evaluated the licensee response to AR A0476360, which described an

intrusion of chlorides into the reactor coolant system.

Observations and Findin s

On February 8, 1999, chemistry personnel identified that, on Unit 1, reactor coolant

system chlorides exceeded the Equipment Control Guideline limitof 150 ppb. The

chloride concentration was 770 ppb and increased until a peak of 1060 ppb was

"

reached.

Chemists sampled the in-service chemical and volume control system

deborating demineralizer and identified that the effluent chloride concentration was

1730 ppb. After operators isolated the in-service deborating demineralizer, the chloride

concentration started decreasing and had returned within the specification of 150 ppb on

February 10. Because reactor coolant system chlorides exceeded the limitby a

significant margin, chemists initiated AR A0476360 to enter this item into the corrective

action system.

-19-

Licensee investigation revealed that a chloride based resin was loaded into the

deborating demineralizer for crud burst cleanup.

However, the barrel in the Diablo

Canyon warehouse was labeled with a licensee material tag stating that the resin was

hydroxide based.

The licensee contacted the resin vendor who confirmed that the barrel

contained a chloride based resin.

Normally, when purchasing resin for use in the reactor coolant system, a receipt

inspection program, which included testing of the resin, was implemented to ensure that

the resin contained no detrimental properties.

The licensee procured the resin as

hydroxide based for use in the radwaste processing system.

Because the resin was

procured for a nonsafety-related

function, no receipt inspection was performed.

The

barrel was labeled as an hydroxide based resin. Chemists noted that this resin was

effective in processing radwaste streams and, therefore, recommended

its use in the

reactor coolant system.

No testing or other confirmatory actions were taken when the

chloride based resin was approved for use in the reactor coolant system.

The licensee initiated Nonconformance Report N0002084 because of the potential

consequences

of the chloride intrusion and the concerns with the resin procurement

process.

The inspectors agreed that the process for dedicating radwaste resin for use

in the reactor coolant system was weak in that no testing or other confirmatory actions

were employed.

The licensee also identified several other barriers that should have

prevented this deficiency.

Procedure OP B-1A:XIII,"CVCS Demineralizers,"

Revision 13, step 1.1, specified, in part, that the demineralizer is to be rinsed and

sampled prior to use.

The effluent was to be routed to the liquid holdup tank while

sampling.

In addition, a CAUTIONprior to Section 2 required verification that samples

are taken to determine the effects of the demineralizer on reactor coolant system

chemistry. The failure of licensee personnel to implement the steps of

Procedure OP B-1A:XIIIis the second example of a violation of Technical Specification 6.8.1.a.

This licensee-identified Severity Level IV violation is being treated

as a noncited violation, consistent with Appendix C of the NRC Enforcement Policy.

This violation is in the corrective action program as Nonconformance Report N0002084

(50-275/99003-02).

Forced oxygenation of the reactor coolant system using hydrogen peroxide was in

progress when the chloride intrusion occurred.

The licensee was initiallyconcerned that

the combination of high oxygen and chlorides in the reactor coolant system could result

in the potential for chloride stress corrosion of reactor coolant system components.

The

licensee contacted the Nuclear Steam Supply System vendor who determined, based

on the actual conditions, chloride stress corrosion was unlikely. The inspectors

reviewed the vendor analysis and concluded that it was satisfactory.

The inspectors

also concluded that the root cause analysis and corrective action process addressed

the

issues appropriately.

Conclusions

The second example of a noncited violation of Technical Specification 6.8.1.a for failure

to follow procedure resulted when chemists failed to sample the chemical and volume

control system demineralizer prior to placing it in service (NCR N0002084).

This error

resulted in a significant chloride intrusion into the reactor coolant system and caused the

-20-

Equipment Control Guideline limitto be exceeded.

In addition, the controls for the

purchase, control, and dedication of resins for nonsafety-related applications were

deficient. The licensee performed a detailed root cause'nalysis

and corrective actions

addressed

the issues appropriately.

S1

Conduct of Security and Safeguards Activities

S1.1

General Comments

71750

During routine tours, the inspectors noted that the security officers were alert at their

posts, security boundaries were being maintained properly, and screening processes

at

the Primary Access Point were performed well. During backshift inspections, the

inspectors noted that the protected area was properly illuminated, especially in areas

where temporary equipment was brought in.

V. Mana ement Meetin s

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management at the

conclusion of the inspection on March 11, 1999. The licensee acknowledged the findings

presented.

The inspectors asked the licensee whether any materials examined during the inspection

should be considered proprietary.

No proprietary information was identified.

0

-1-

ATTACHMENT

SUPPLEMENTAL INFORMATION

PARTIALLIST OF PERSONS CONTACTED

Licensee

J. R. Becker, Manager, Operations Services

W. G. Crockett, Manager, Nuclear Quality'Services

R. D. Gray, Director, Radiation Protection

T. L. Grebel, Director, Regulatory Services

D. B. Miklush, Manager, Engineering Services

D. H. Oatley, Vice President and Plant Manager

R. A. Waltos, Manager, Maintenance Services

L. F. Womack, Vice President, Nuclear Technical Services

INSPECTION PROCEDURES (IP) USED

IP 37551

IP 61726

IP 62707

IP 71707

IP 71750

IP 92700

IP 92901

IP 92902

IP 92903

IP 92904

IP 93702

Onsite Engineering

Surveillance Observations

Maintenance Observation

Plant Operations

Plant Support Activities

Onsite Followup of Written Reports of Nonroutine Events at Power Reactor

Facilities

Followup - Operations

Followup - Maintenance

Followup - Engineering

Followup - Plant Support

Prompt Onsite Response

to Events at Operating Power Reactors

ITEMS OPENED AND CLOSED

~oened

None.

Closed

50-275/97003-04

50-275/97-004-01

50-275/95-013-02

and -01

VIO

failure to take adequate corrective actions to correct

deficiencies in the painting program (Section M8.1)

LER

Technical Specification 3.7.1.2 not met because

of paint

applied to auxiliary feedwater pump turbine governor

linkage (Section M8.2)

LER

component cooling water system may have operated

outside of its design basis (Section E8.1)

.

0 ened and Closed

50-275/99003-01

50-275/99003-02

50-275/99003-03

50-275; 323/

99003-04

NCV

Improper maintenance clearance preplanning on nitrogen

system during midloop and for relay replacement

(Sections 01.2 and M1.3)

NCV

Failure to enable RVRLIS alarm during midloop and failure

to sample demineralizer as required (Sections 01.2

and R1.1)

NCV

Inadequate maintenance procedure resulted in partial loss

of offsite power (Section M1.4)

NCV

Failure to submit license amendment for changes to 230 kV

offsite power system (Section E1.2)

LIST OF ACRONYMS USED

AR

DEG

IP

NCV

NRC

PDR

RHR

RVRLIS

VIO

action request

diesel engine 'generator

inspection procedure

noncited violation

Nuclear Regulatory Commission

Public Document Room

residual heat removal

reactor vessel refueling level indication system

violation