ML16342E128

From kanterella
Jump to navigation Jump to search
SALP Repts 50-275/98-99 & 50-323/98-99 for 960818-980509
ML16342E128
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 06/15/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML16342E129 List:
References
50-275-98-99, 50-323-98-99, NUDOCS 9806230118
Download: ML16342E128 (12)


See also: IR 05000275/1998099

Text

IIIW

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE (SALP)

Report 50-275/98-99; 50-323/98-99

I.

BACKGROUND

The SALP Board convened on May 12, 1998, to assess

the nuclear safety performance of the

Diablo Canyon facilityfor the period of August 18, 1996, through May 9, 1998. The Board

Meeting was conducted in accordance with Management Directive 8.6, "Systematic Assessment

of Licensee Performance."

The Board members were K. E. Perkins (Board Chairperson),

Director, Walnut Creek Field Office, Region IV; D. D. Chamberlain, .Deputy Director, Division of

Reactor Safety, Region IV; and W. H. Bateman, Director, Project Directorate IV-2, Office of

Nuclear Reactor. Regulation.

This assessment

was reviewed and approved by the Region IV

Administrator.

in

Plant Operations

Maintenance

Engineering

Plant Support

2

1

2

1

~rv~iu

II.

PLANT OPERATIONS

Overall performance in Plant Operations improved during this assessment

period. The licensee

continued to demonstrate the strengths observed during the previous assessment

and took

actions to address previous weaknesses;

however some actions were not fullyeffective.

Management oversight was generally effective, resulting in conservative decision making and a

strong focus on safety.

Operator response to events and abnormal conditions continued to be

strong, although performance during routine evolutions revealed instances of inadequate

communications, inattention to detail, and procedural noncompliance.

Continued weakness was

observed with the proper implementation of the clearance process.

In addition, shift turnover

practices by licensed operators and shift supervision were considered weak. Operator training

remained effective, and audits of the operations department generally resulted in management

taking effective corrective'actions.

Management oversight was generally effective, resulting in conservative decision making and a

strong focus on safety. The focus on safety was particularly evident when power reductions

were initiated for anticipated adverse weather conditions, for offsite grass fires that potentially

threatened power lines, and for emerging equipment problems.

Management was involved in

planning and direct oversight of significant evolutions, including midloop operations during the

Unit 2 outage.

An exception occurred during the Unit 2 startup transformer replacement when

NRC involvement was necessary to ensure that management

adequately considered

contingency plans.

Management was sensitive to conditions affecting operators as evidenced

by their control of potential maintenance distractions, emphasis on correcting control room

deficiencies, moving the shift foreman into the control room, and reducing the amount of

paperwork reviewed in the control room. Management took action since the last assessment

to

9806230ii8 9806i5

PDR

AOGCK 05000275

G

POR

-2-

provide consistent performance expectations

in most areas, but had not developed full staff

acceptance or implementation of those expectations.

Problems with procedure adherence

and

clearance control continued to occur although to a lesser extent.

Operator response to events and abnormal conditions continued to be strong.

Operators

performed well when faced with main feedwater pump problems and the inadvertent isolation of

a main steam line. In addition, operators effectively performed several power level changes

in

response to external events and to permit maintenance activities. Control room command and

control improved as a result of implementing new standards for communications, peer and

self-checking, and reactivity control. Despite the general improvements observed in control

room work practices, the conduct of shift turnovers was observed to be weak in that operators

did not perform thorough control board walkdowns and shift supervisors did not consistently

enter the main control room area during their shift tumovers.

Some problems occurred

during

routine evolutions which typically resulted from a lack of thorough communications and

inattention to detail.

In addition, procedure adherence problems continued to occur, and in one

noteworthy instance,

a licensee quality evaluation report identified that two senior reactor

operators deliberately deviated from procedures.

Although the licensee generally observed a lower number of significant clearance errors during

the assessment

period, incidents of significant clearance errors continued.

These incidents

included three occurrences where all of the barriers imposed to protect personnel and

equipment were ineffective and other instances where multiple barriers were ineffective. These

incidents did not result in personnel injury or equipment

damage, but indicate'd that revisions to

the clearance procedure to simplify implementation of the clearance process were not fully

effective.

Overall, training of operations staff continued to be effective, and requalification examinations

were challenging and well constructed.

Training conducted prior to the Unit 2 outage provided

valuable lessons to the operators and identified necessary

procedure changes.

A training,

program weakness

in tracking qualification status resulted in some operators not completing the

annual refresher for self-contained breathing apparatus and many operators not having the

appropriate corrective lenses for use with the equipment.

Nuclear Quality Services audits were of high quality, and corrective actions were generally

effective. Operations'elf-assessments

improved but were not consistently self-critical of

performance.

Finally, personnel in the operations department demonstrated

a good

understanding of the corrective action process, and the process was used effectively to identify

and correct deficiencies.

Performance

in the Plant Operations functional area was determined to be Category 2.

III.

NlAINTENANCE

Maintenance performance improved during this assessment

period and attained a superior level

during the latter portion of the period. Management effectiveness and support were improved,

oversight was effective, and decision making was conservative.

The maintenance and

-3-

surveillance program and procedures were well established and effective for routine activities,

but in some instances nonroutine activities were not well controlled. Conduct of maintenance

and surveillance activities was generally strong, with isolated procedure compliance and

implementation problems.

Maintenance backlogs were significantly reduced over the

assessment

period and were effectively controlled. Material conditions continued to improve

and were considered excellent, especially for safety related equipment.

The technical capability

of craft personnel remained high, which indicated effective training and qualification programs.

Performance assessment

programs were considered excellent.

Management involvement and support were effective during this period. Supervision was

routinely involvedin field observations,

in evaluation of "as found" conditions, and in

determinations of appropriate corrective actions.

Conservative decision-making was

demonstrated

by the prudent decision to defer the second Unit 2 transformer outage because of

poor weather conditions.

Relatively isolated procedure compliance and implementation errors

occurred during this assessment

period, and maintenance services recently implemented a

formal process for management field observations to further reduce errors.

The maintenance and surveillance program and procedures were well established and

effectively controlled most activities. Earlier in the assessment

period, the maintenance

rule

baseline inspection identified some problems, primarily related to the application of the risk

aspects of the program, which were effectively addressed

later in the period. Some nonroutine

maintenance activities were not well controlled with appropriate procedures or oversight.

Examples included a procedure which failed to require a post maintenance test to demonstrate

that auxiliary saltwater system check valves were properly installed, a failure to ensure proper

oversight and current training of a contractor installing a ground buggy, and a failure to instruct

personnel to use caution in removing scaffolding when working near the main steam isolation

valves.

In the latter case, personnel working near the main steam isolation valves inadvertently

caused a reactor trip and subsequent

safety injection actuation.

The conduct of maintenance and surveillance activities was generally strong.

Performance

problems appeared to decline over the assessment

period, and many of those that occurred

were self-identified, reported, and effectively corrected by the licensee.

Improvements were

noted in reducing the number of clearance errors, but some significant errors occurred

through

the end of the assessment

period, warranting continued management attention.

In addition,

there was an instance of inappropriate painting activities which caused a turbine driven auxiliary

feedwater pump to be degraded.

Right after the end of the assessment

period, the continued

need for management

attention to conduct of maintenance was evidenced when oil was drained

from the wrong auxiliary feedwater pump.

The overall material condition of the facility continued to improve over the assessment

period

and was considered excellent. A notable example was the intake structure and equipment.

Balance of plant material condition was improved, but isolated controller problems with the main

feedwater pumps continued to occur.

Maintenance backlogs were significantly reduced over the

assessment

period and were considered effectively controlled during the latter portion of the

period.

The technical capability of the craft personnel remained high. Training and qualification of

maintenance and surveillance personnel was considered effective. A challenge for the licensee

willbe to continue the trend in reduced procedure compliance problems and isolate performance

errors noted toward the end of the assessment

period as they implement planned organizational

changes.

Performance assessment

programs in the form of audits and department self-assessments

were

considered excell nt. Problem identification through the corrective action process was effective

with the licensee routinely self-identifying and correcting problems.

Intrusive and self-critical

audits were performed to identify both strengths and weaknesses

in the maintenance and

surveillance programs.

Performance

in the Maintenance functional area was determined to be Category 1.

IV.

ENGINEERING

Engineering performance was good with improvement noted during this assessment

period.

Management initiatives were effective in addressing many of the issues raised during the

previous assessment

period. The consolidation of engineering into a single onsite organization

has presented management challenges.

Procedures

and programs were effective, but some

process modification was needed to address the regulatory aspects of design changes and

design basis fidelityearlier and more effectively. Technical adequacy of the engineering

organization was a strength when the organization was focused.

Engineering support to

operations and maintenance was good.

Insightful results from quality organization audits were

utilized to strengthen engineering.

Management was effective in this assessment

period in reviewing and prioritizing the large

engineering backlog.

Some items were eliminated, and a large number were worked such that

only a small number of quality-related items remained.

Management initiated a quality plan

program that enabled engineering to better track its performance and identify areas of resource

need.

To facilitate consolidation of engineering onsite, management developed innovative

initiatives to retain design basis corporate knowledge, assure effective knowledge transfer, and

centralize various data bases.

The ongoing consolidation of engineering onsite warrants

continued management

attention.

Procedures were effective with only a few exceptions noted.

Most programs were effective in

accomplishing their objectives.

Weaknesses

were evident, however, in the 10 CFR 50.59 and

design basis fidelity programs.

Regulatory aspects of design changes were not always

adequately addressed

in reviews performed under the 10 CFR 50.59 program.

This was evident

in the instances of reviews that raised concerns regarding potential unreviewed safety

questions.

Problems with the Updated Final Safety Analysis Report (UFSAR) update programs

related to design basis fidelity continued to be identified by the licensee and the NRC, and

indicated weaknesses

in the licensee's sampling approach to this issue.

The architect engineering inspection confirmed the high quality of engineering work.

Engineering technical competence was a strength when management

ass'ured issues received

-5-

an appropriate focus.

However, some instances of late identification or slow resolution of

issues during this assessment

period were identified and necessitated

NRC involvement. The

issue involving operability of the auxiliary saltwater system floor drain check valves was

identified by the licensee but required NRC involvement to assure prompt resolution.

Engineering support to operations and maintenance was generally good. An engineering fix-it-

now team was formed to be more responsive to daily issues, and engineering supported

the

evolving facility asset teams.

Operability evaluations were improved from the last assessment.

Technically sound and timely resolution of issues was characteristic of system engineering.

However, the licensee was occasionally slow to address self-identified issues such as

abnormally high concentration ofwater in the governor of a turbine driven auxiliary feedwater

pump. Weaknesses

identified in system engineering knowledge of the Maintenance Rule during

the NRC's baseline inspection were promptly corrected.

The quality assurance

organization and the independent safety engineering group were

aggressive in performance oftheir responsibilities.

Their audits were rigorous and critical.

Engineering's use of audit and self-assessment

results was fundamental to the improvements

made during this period. Corrective actions were tracked and were generally effective although

not always timely.

Performance in the Engineering functional area was determined to be Category 2.

V.

PLANT SUPPORT

Overall performance in the Plant Support area continued to be superior with several

improvements noted during the assessment

period.

Performance

in the radiological controls

area was strong with outstanding performance noted in reducing person-rem exposures for plant

workers.

Emergency preparedness

performance continued to be strong. The security area

performance issues noted in the last assessment

were effectively addressed

during this period

and performance was considered excellent.

Housekeeping at the facilitywas very good.

Fire

protection program implementation continued to be generally strong.

Performance assessment,

problem identification, and corrective action effectiveness were excellent, although timeliness of

corrective actions for identified problems could be improved in some areas.

Superior performance was noted in the radiological controls area during this assessment

period.

Management provided strong support for an extended (approximately 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />) reactor

shutdown chemistry initiative, which combined with the installation of additional temporary

shielding and emphasis on maintaining exposures ALARA,resulted in significant improvement in

person-rem exposures

at the facility. The 3-year person-rem exposure average for the facility

was better than the national average for pressurized water reactors.

Personnel contamination

events, contaminated surface areas, generation of radioactive waste, and incidents of

contamination found outside the radiological controlled area were reduced during the

assessment

period indicating effective controls in those areas.

Overall, excellent programs were

effectively implemented for radioactive waste eNuent management,

solid radioactive waste

management,

radioactive material transportation, and environmental monitoring. Excellent

performance was noted in the reduction of airborne noble gas, iodines, particulates, and liquid

-6-

mixed radionuclides.

Chemistry performance at the facility has historically been strong and

continued at a superior level during this assessment

period.

Effective self-assessment

programs were in place in the radiological controls area.

Self-assessment

findings and other

identified problems were generally effectively addressed

in a timely manner, although initial

actions to correct a problem with personnel entering the radiological controlled area without

appropriate dosimeters were not fullyeffective. Performance at the end of the assessment

period indicates that the licensee has been effective in addressing this issue.

Emergency preparedness

performance continued to be strong during this assessment

period.

Performance during the simulator walkthrough inspection and during the biennial exercise was

considered very good. Actual events which occurred during the period were properly classified

and offsite agency initial notifications were timely. The emergency preparedness

training

program was well implemented and training was effectively tracked.

Program enhancements,

including a job task analysis, lesson plan upgrades, and increased drill frequency demonstrated

a high level of management support. Although strong performance was noted overall, some

problems were noted with incomplete lessons-learned

documentation for two actual events and

with untimely response to some emergency preparedness

corrective action requests.

Security performance improved over this assessment

period and was considered excellent.

The

performance issues noted in the security area during the last assessment

period were effectively

addressed

during this period. Areas which improved included searching material entering the

protected area, implementing the access authorization program, and reducing the number of

vital area alarms.

Program strengths were noted in the security backup power supply system,

radio communications system, and the records and reports programs.

An Operational

Safeguards Response

Evaluation (OSRE) determined that the security force demonstrated

excellent contingency response capability. Late in the assessment

period, an issue was

identified regarding changes made in the deployment of armed response officers. The licensee

committed to address the issue by maintaining response as demonstrated

during the OSRE.

The installed vehicle barrier was evaluated as capable of protecting required plant vital

equipment from a vehicle bomb threat.

The security testing and maintenance program was

generally effectively and properly documented although some action requests were not

completed in a timely manner.

Housekeeping at the facilitywas considered very good. The fire protection program and its

implementation continued to be strong during this assessment

period.

Fire protection program

audits were found to be self-critical and aggressive.

Fire brigade and fire watch personnel were

very knowledgeable of their assigned duties. The licensee effectively controlled transient

combustibles with the exception of some isolated problems at the intake structure.

Fire barriers

were appropriately maintained and the licensee had an aggressive program to correct identified

problems with penetration seals.

Licensee response to a fire during the assessment

period was

effective.

Performance assessment

programs in the form of audits and internal self-assessments

were

considered

a strength.

Problem identification and corrective action effectiveness were generally

strong although timeliness of corrective actions for identified problems could be improved in

some areas.

Performance in the Plant Support functional area was determined to be Category 1.