ML16342D491

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Insp Repts 50-275/96-21 & 50-323/96-21 on 960929-1109. Violation Noted.Major Areas Inspected:Operations,Maint & Engineering
ML16342D491
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 12/04/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML16342D489 List:
References
50-275-96-21, 50-323-96-21, NUDOCS 9612100275
Download: ML16342D491 (60)


See also: IR 05000275/1996021

Text

ENCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket Nos.:

50-275, 50-323

License Nos.:

DPR-SO, DPR-82

Report No.:

50-275/96021, 50-323/96021

Licensee:

Pacific Gas and Electric Company

Facility:

Diablo Canyon Nuclear Power Plant, Units

1 and 2

Location:

Dates:

7 1/2 miles NW of Avila Beach

Avila Beach, California

September 29, 1996, to November 9, 1996

Inspectors:

Approved By:

M. Tschiltz, Senior Resident Inspector

S. Boynton, Resident Inspector

M. Runyan, Reactor Inspector, Region IV

C. Myers, Reactor Inspector, Region IV

D. Allen, Reactor Inspector, Region IV

R. Huey, Acting Chief, Branch E

Division of Reactor Projects

ATTACHMENT:

Supplemental Information

9612100275

961204

PDR

ADQCK 05000275

8

PDR

)

-2-

EXECUTIVE SUMMARY

Diablo Canyon Nuclear Power Plant, Units

1 and 2

NRC Inspection Report 50-275/96021; 50-323/96021

~Oeretione

PGRE failed to perform safety evaluations,

in accordance with 10 CFR 50.59 when

revising the emergency operating procedure

(EOP) for transferring the emergency

core cooling system (ECCS) from the injection to recirculation mode following a loss

of primary coolant.

As a result, no evaluation was performed to determine if the

differences between the EOP and the Updated Final Safety Analysis Report (UFSAR)

constituted an unreviewed safety question.

An apparent violation was identified

(Section 01.2).

Operators failed to recognize, for existing plant conditions, that removal of a

centrifugal charging pump (CCP) from service required entry into a Technical

Specification (TS) action statement for the charging pumps approximately 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />

into the allowed 72-hour action time. This was considered to be an example of

operator inattention to detail.

Although no violation of (TS) requirements occurred,

insufficient corrective actions were taken to address this issue until questioned by

the NRC (Section 01.3).

Maintenance

Operators did not document a sticking solid state protection system test reset

switch, following identification of the problem during routine surveillance testing.

A

noncited violation was identified (Section M1.2.1).

Performance criteria established for main steam safety valves (MSSVs), in

accordance with the maintenance

rule, did not adequately define the valve

performance necessary to assure that the MSSVs were capable of performing their

intended safety function. A violation was identified (Section M8.1).

The licensee identified that MSSVs were incorrectly set during periodic testing due

to setpressure

inaccuracy introduced by the use of valve specific correction factors.

As a result, on 53 different occasions,

MSSV's were returned to service set outside

of the a1 percent tolerance required by TS. A noncited violation was identified

(Section M8.1).

Enrnineering

~

Three examples of a weakness

in the licensee's

procedure review and revision

process were identified. The examples involved conflicting requirements for control

of charging pumps in the Unit 2 procedure for cooldown to cold shutdown (Section

0

-3-

01.3), inaccurate reference to TS requireme'nts

in a local leak rate testing procedure

(Section M1.2.2), and inappropriate deletion of steam flow/feed flow mismatch

setpoint calibrations from a surveillance procedure (Section M1.2.3).

~

The Plant Staff Review Committee (PSRC) inappropriately approved

a TS

interpretation which, although meeting the intent of the TS, allowed measured,

controlled leakage in excess of the 40 gpm limit specified in the TS (Section E8.1).

Careful monitoring of residual heat removal (RHR) pump oil additions by the system

engineer identified oil leakage which identified a pump operability problem that was

effectively evaluated and corrected (Section E1.1).

0

Re ort Details

Summar

of Plant Status

Unit

1 began this inspection period at 100 percent power.

On November 3, the unit was

curtailed to 50 percent to clean the main condenser waterbox.

The unit was returned to

100 percent power on November 4, and remained there for the balance of the inspection

period.

Unit 2 began this inspection period at 100 percent power.

On November 2, power was

reduced to 50 percent, when several of the reheat stop valves failed to reopen during

periodic surveillance testing.

Following associated

repairs, the unit was returned to

100 percent power on November 3, and remained there for the balance of the inspection

period.

I. 0 erations

01

Conduct of Operations

01.1

General Comments

71707

Using Inspection Procedure 71707, the inspectors conducted frequent reviews of

ongoing plant operations.

In general, the conduct of operations was professional

and safety-conscious.

Operators were knowledgeable of the status of plant

equipment.

Inspectors noted that there continues to be approximately 190 Action

Requests

(ARs) written on monitored equipment, controlled and/or operated from

the control room.

In discussions with licensee management,

the inspector

confirmed that PGSE has an ongoing initiative to reduce the number of outstanding

control room ARs. The licensee's

planned actions to actively monitor and track the

backlog of control room deficiencies, appeared to be both warranted and

appropriate.

01.2

EOP E-1.3 Transfer to Cold Le

Recirculation

a.

Ins ection Sco

e 71707 37551

F

As part of a review of the RHR system, the inspector reviewed the licensee's

emergency procedure for transition from the injection mode to the cold leg

recirculation mode following a loss of primary coolant.

The review included the

following documents:

UFSAR, Section 6.3

Procedure

E-1.3, Rev. 14, "Transfer to Cold Leg Recirculation"

Design Criteria Memorandum S-9, Safety Injection System

NUREG-0675, Safety Evaluation Report related to the operation of Diablo

Canyon Nuclear Power Station Units

1 and 2, Supplement 9.

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Observations

and Findin s

UFSAR

Regulatory Guide (RG) 1.70, Revision 1, "Standard Format and Content of Safety

Analysis Reports for Nuclear Power Plants," specifies that the UFSAR include a

discussion of the ECCS capability to meet functional and performance requirements

over both the short and long term duration of an accident, including specific

features (e.g. switchover to different coolant delivery paths) provided to meet such

requirements.

In addition, RG 1.70 specifies that (1) the UFSAR shall identify all

manual actions required to be taken by an operator in order for the ECCS to perform

properly; and (2) a discussion shall be included in the UFSAR to describe the

information available to the operator, the time delay during which the operator's

failure to act properly will have no unsafe consequences,

and the consequences

if

the action is not performed.

Section 6.3.1.4.4.2 of the UFSAR, describes the changeover of ECCS from injection

mode to recirculation mode after a loss of primary coolant.

The section describes

that upon receipt of the refueling water storage tank (RWST) low level alarm

(33 percent),

a signal is provided to trip both RHR pumps.

The remainder of the

changeover sequence

is accomplished manually by the operator from the control

room. The sequence

of steps for the manual changeover

and the approximate times

to complete those steps are provided in Tables 6.3-4 and 6.3-5. As shown in

Table 6.3-5, the total time required to switchover to the cold leg recirculation mode

is approximately 10 minutes, based upon the sequence

of steps delineated

in

Table 6.3-4.

The time available to the operators is also described by the timing

difference between reaching the RWST low level alarm and the low-low level alarm.

Table 6.3-5 states these times as 17 minutes and 39 minutes, respectively, for an

available time of 22, minutes.

In Supplemental Safety Evaluation Report 9, dated June 1980, the NRC reviewed

the licensee's

analysis of available time for operator response

and the switchover

actions required for cold leg recirculation.

The NRC concluded that the proposed

manual procedure,

as described

in the UFSAR, with the automatic trip of the RHR

pumps was acceptable.

The inspectors noted the staff's acceptance

of the manual switchover was

conditional in that it required the licensee to more fully automate the switchover

process.

The details of the requirement to automate the transfer to cold leg

recirculation were specified in a letter from A. Schwencer, Chief, Licensing Branch

No. 3, Office of Nuclear Reactor Regulation, to M. Furbush, Vice President and

General Counsel, Pacific Gas and Electric Company, dated May 7, 1980.

The

licensee responded

in a letter dated May 28, 1980, requesting clarification on the

requirement and a meeting with the NRC staff.

Subsequent

to the May 28 letter,

no action was taken by the licensee to more fully automate the ECCS transfer to

cold leg recirculation.

To date, the licensee has been unable to locate

-3-

documentation regarding any further action on this matter.

The licensee has been

requested to address this matter in the predecisional enforcement conference.

Desi

n Criteria Memorandum

Design Criteria Memorandum (DCM) S-9, Safety Injection System, states that during

the licensing process, the information in the UFSAR Tables 6.3-4 and 6.3-5 were

developed to demonstrate that the manual switchover could be performed before

the operating ECCS pumps lost suction from the RWST. The DCM further states

that PGRE calculation N-095 determined the minimum time available for switchover

to cold leg recirculation.

The calculation determined that with both ECCS trains

operating, the RHR pumps trip on RWST low level at 13 minutes and the RWST

low-low level is reached

in 28 minutes.

This provides a minimum available

switchover time of 15 minutes.

Although these timeframes differ from those in

Table 6.3-5, the table was never updated to reflect the current calculation.

Emer enc

Procedure

EP

OP 1.3 and EOP E-1.3

Another procedure,

EP OP-1.3, which was also entitled "Transfer to Cold Leg

Recirculation," was implemented in 1984 to incorporate the Westinghouse Owner's

Group Emergency Response

Guidelines for the transition of ECCS systems from

injection to cold leg recirculation.

Although the procedure history sheet for

Revision 0 of EP OP-1.3 identified that the procedure was described in the UFSAR,

the differences between the procedure described

in the UFSAR and EP OP-1.3 were

not evaluated

in accordance with 10 CFR 50.59.

In 1985, EOP E-1.3 was issued and superseded

EP OP-1.3.

Procedure

EOP E-1.3

is the current implementing procedure for the transition of ECCS from the injection

mode to the cold leg recirculation.

A review of Procedure

EOP E-1.3 found that it

differed in content and sequence

from the procedure described

in the UFSAR.

Review of the procedure history sheets,

associated with the original version of

Procedure

EOP E-1.3 and its 14 subsequent

revisions, identified that evaluations of

the changes were required in accordance with 10 CFR 50.59, although none had

been performed.

Based upon other previously raised concerns regarding the accuracy of the UFSAR,

the licensee had previously initiated a programmatic review of all sections of the

UFSAR. Although this review was completed and areas requiring change identified,

it failed to identify the differences between Section 6.3 of the UFSAR and

EOP E-1.3.

The significance of the licensee's failure to evaluate the changes against the

licensing basis in the UFSAR, is that several of the changes increased the time it

would take operators to complete the switchover from injection to recirculation

following a loss of coolant accident (LOCA). This reduced the time margin available

before the ECCS pumps would lose suction from a low-!ow water level condition in

the RWST (4 percent level). That time margin was, in part, the basis for the NRC's

acceptance

of the manual switchover procedure

as documented

in SSER 9.

The inspector questioned the licensee on the impact of the changes to Procedure

EOP E-1.3, upon the times listed in Table 6.3-5 of the UFSAR.

In response to this

question, the licensee performed a prompt operability assessment

(POA) that

evaluated the differences between the UFSAR and EOP and analyzed the time

available to the operator to complete the switchover.

The evaluation noted that

changes

had been made which added steps to the EOP and changed the sequence

of some steps.

The POA, documented

in AR A0416238, determined that with the

conservatisms

in the UFSAR removed, it would take 16.2 minutes to empty the

usable volume of the RWST following the automatic trip of the RHR pumps.

The

POA noted that gas binding of the CCP, containment spray pumps, and safety

injection pumps would occur if the RWST were to empty before the transfer to cold

leg recirculation was completed.

This condition could potentially damage the pumps

and would necessitate

venting of the pumps suction piping.

Corrective Actions

In response to the inspectors'oncerns

regarding the differences between

Procedure

EOP E-1.3 and the UFSAR, and the impact of the differences on the

operator's ability to transfer to cold leg recirculation prior to reaching

a low-low

level condition in the RWST, the licensee initiated several corrective actions.

To

ensure the transfer could be performed in an acceptable

period of time (i,e. prior to

receiving the RWST low-low level alarm), the Operations Director issued

a standing

order directing that the transition to EOP E-1.3 not be delayed for the conduct of a

tailboard, and that stroking of valves need not be completed prior to proceeding to

the next step.

The guidance in the standing order for valve stroking is consistent

with the Westinghouse

Owners Group Emergency Response

Guidelines Users

Guide.

Utilizing the guidance, several operating crews demonstrated,

on the plant

simulator, that the switchover could be performed in approximately 10 minutes.

Based upon the questions and concerns raised by the inspector, the licensee has

initiated another comprehensive review of the UFSAR to determine what other

operational procedures

or tasks are described therein, and to evaluate their

consistency with existing plant procedures,

as applicable.

The licensee performed a

10 CFR 50.59 review of the changes

and determined that an unreviewed safety

question does not exist.

Additionally, the licensee is conducting

a review of EOP

E-1.3 in order to r'evise the procedure

as needed.

Conclusions

The compensatory actions taken by the licensee, for the implementation of

Procedure

EOP E-1.3, adequately ensured that the transfer to cold leg recirculation

could be completed in a time frame consistent with the UFSAR. However, the

multiple failures (from 1984 to 1996) of the licensee to evaluate the impact of the

revisions to Procedure

EOP E-1.3 on the plant's licensing basis, is indicative of a

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potentially significant problem with the implementation of the requirements of

10 CFR 50.59.

Additionally, as a result of differences between the EOP E-1.3 and

the UFSAR, an extensive evaluation was required for the licensee to establish

a

reasonable

expectation that an unreviewed safety question did not exist.

This is an

apparent violation of 10 CFR 50.59 (EEI 50-275;323/96021-01).

01.3

Confi uration Control of CCPs

Ins ection Sco

e 71707

The inspector reviewed the licensee's controls of CCPs during shutdown conditions.

This review included the following procedures:

STP l-1A, Revision 58, Routine Shift Checks Required by Licenses.

OP L-5, Revision 24, Plant Cooldown From Minimum Load to Cold

Shutdown.

OP1.DC17, Revision 2A, Control of Equipment Required by the Plant TS.

OP1.DC37, Revision 4B, Plant Logs.

OM7.ID1, Revision 6, Problem Identification and Resolution.

b.

Observations

and Findin s

Technical Specification 3.1.2.4 requires two charging pumps to be operable while

the plant is in Modes 1-4. TS 3.1.2A also requires that one of the CCPs be

rendered inoperable when the lowest reactor coolant system (RCS) cold leg

temperature

is equal to less than 270'F.

TS 3.1.2.3 requires one charging pump to

be operable with an operable emergency power source when the plant is in Modes

5 and 6. When in Modes 5 and 6, the TS further requires that all CCPs, other than

the required operable pump, be rendered inoperable.

Both TS surveillance

requirements 4.1.2.3.2 and 4.1.2.4.2 require all of the CCPs, other than the

required operable charging pump(s), to be verified inoperable every 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> by

verifying that the motor breaker DC control power is deenergized.

Operating Procedure

(OP) L-5 describes the sequence

of steps necessary to bring

the plant to a cold shutdown condition. Instructions in OP L-5 provide for removing

the charging pumps from service in accordance with TS 3.1.2.3 and 3.1.2.4 to

ensure low temperature overpressure

protection.

Step 6.2.20 directs operators to

disable one of the CCPs upon entry into Mode 4 with RCS cold leg temperature

greater than 270'F.

Step 6.3.10 directs operators to disable a second charging

pump while in Mode 5 prior to RCS temperature falling below 161.9'F.

-6-

0 erator Reco

nition of Entr

Into TS Action Statement

A review of operating logs for the Unit 2 shutdown for refueling outage 2R7 found

that, prior to the commencement of the shutdown, the PDP was removed from

service for maintenance.

During the RCS cooldown in Mode 4, operators rendered

CCP 2-2 inoperable in accordance with Procedure

OP L-5 and TS 3.1.2.4, prior to

RCS cold leg temperature falling below 270

F. However, the operators failed to

recognize that with the PDP inoperable, they no longer met the limiting condition for

operation of TS 3.1.2.4.

Entry into the action statement for TS 3.1.2.4 was not

identified until two days later when a new operating crew came on shift. At that

time, a TS tracking sheet was initiated in accordance with Procedure OP1.DC17,

and appropriately backdated to the time the CCP was rendered inope'rable.

The

action statement for TS 3.1.2.4 allows 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> to restore

a charging pump to

operable status.

The plant entered Mode 5 prior to the 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> action time being

exceeded,

and therefore,

a violation of the TS did not occur.

The licensee initiated an event trending record (ETR) to track this issue for adverse

trends.

The ETR was evaluated by the Operations Director who determined that an

AR was not required.

Procedure OM7.ID1 provides guidance on what problems

require documentation in an AR. However, no specific examples are provided for

the failure of operators to recognize and enter into a TS action statement.

The

inspectors questioned the Operations Manager and Operations Director on the need

to utilize the AR process to ensure that the operators'ailure

to recognize entry into

a TS action was properly dispositioned for corrective action.

The Operations

Manager noted that, in hindsight, the issue should have been tracked through the

AR process recognizing that Procedure

OM7.ID1 did not specifically require it. He

further noted that it was his expectation that if there are similar occurrences

in the

future, an AR would be initiated.

The licensee recently implemented programmatic actions to improve operations

performance.

These actions, described in the operations quality plan, include 1)

improved formality in the control room, 2) development of crew performance

metrics, 3) reemphasis

on the need for attention to detail in the control of TS

required equipment, and 4) implementation of three-way communications.

These

actions address,

in part, the operators'ailure to enter into the action statement for

TS 3.1.2.4 and should preclude recurrence of similar problems.

OP L-5 Inconsistenc

with TS

During the review of Procedure

OP L-5, it was noted that Step 6.3.10 in the Unit 2

procedure differed from Step 6.3.10 in the Unit 1 procedure.

Specifically, the Unit

2 procedure contained an additional option for rendering the second charging pump

inoperable by closing the manual discharge isolation valve for the pump.

This

option, which was not provided in the Unit 1 procedure, was inconsistent with the

TS surveillance requirements of 4.1.2.3.2 which specify that the pump be rendered

inoperable by deenergizing

DC control power to the motor breaker.

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-7-

Step 6.3.10 also requires the inoperable pump to be caution tagged in accordance

with Attachment 9.4 of the procedure.

Attachment 9.4 of the Unit 2 procedure did

not provide an option for the operators to caution tag the manual discharge isolation

valve. Additionally, Procedure

STP l-1A, which implements the surveillance

requirements of TS 4.1.2.3.2, only directs the operator to verify that the breaker

DC control power is deenergized.

Therefore, it is likely that an operator who chose

the inconsistent option would have uncovered the problem during the course of

performing Attachment 9.4 or performing STP I-1A. The inspectors noted no

instances of power not being deenergized for past occasions requiring the charging

pump to be rendered inoperable.

During discussions with individuals in the operations department, it was noted that

the additional option in the Unit 2 procedure had been inadvertently added during a

recent revision, and was not identified as conflicting with the TS during the review

and approval process.

Since this issue was brought to the attention of PGRE management,

an on-the-spot

change to the Unit 2 Procedure

OP L-5 was written and issued to remove the option

of closing the manual discharge isolation valve.

Conclusions

Operators did not recognize entry into a TS action statement for the charging pumps

for approximately 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> during the unit shutdown for refueling outage 2R7. This

was considered by the inspectors to indicate inattentive watchstanding by both the

control room operators and operations shift management.

Although the licensee

has taken corrective actions to address the general area of inattentive

watchstanding,

actions taken in response to this specific event were considered

weak.

The incorporation of conflicting requirements into Procedure

OP L-5 for Unit 2 was

considered

a weakness

in the implementation of the licensee's

procedure revision

and review process.

08

lVliscellaneous Operations Issues (92901)

08.1

Closed

Violation 50-323 95018-02: failure to document the basis for the

operability of a degraded reactor cavity sump level indication.

The licensee

determined the root cause of the violation to be personnel error with regards to the

assessment

and handling of the degraded condition.

The licensee's corrective

actions included discussions of the event with other shift supervisors.

Expectations

for involving management

earlier in the operability determination process

and

making timely and conservative operability determinations were reemphasized.

The

licensee also implemented several other corrective actions, including a design

change to the level instrument, to improve the reliability of the sump level

indication.

The licensee's actions to address the root cause of the violation appear

to be adequate to prevent its recurrence.

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II. IVlaintenance

M1

Conduct of Maintenance

M1

~ 1

Maintenance Observations

Ins ection Sco

e 62707

The inspectors observed

all or portions of the following work activities:

C0146283

Replace Valve MS-1-100 (Unit 1)

R0164338

Routine Maintenance of Station Battery Charger 1-2 (Unit 1)

C0147463

Repair Seal Water Pipe to Pump Leak on Auxiliary Feedwater

Pump 2-1 (Unit 2)

C0147S02

Replace Pressurizer Heater Breaker 52-23E-05 (Unit 2)

b.

Observations

and Findin s

The inspectors found the work performed under these activities to be properly

accomplished

in accordance with procedures.

All work observed was performed

with the work package present and in active use.

Technicians were experienced

and knowledgeable of their assigned tasks.

The inspectors observed the system

engineer monitoring job progress during the replacement of the pressurizer heater

breaker.

The Technical Maintenance technician appropriately contacted the system

engineer to resolve problems encountered

during the testing of the replacement

breaker.

When applicable, appropriate radiation control measures were in place.

M1.2

Surveillance Observations

a.

Ins ection Sco

e 61726

Selected surveillance tests required to be performed by the TS were reviewed on a

sampling basis to verify that (1) the surveillance tests were correctly included on

the facility schedule;

(2) a technically adequate

procedure existed for the

performance of the surveillance tests; (3) the surveillance tests had been performed

at a frequency specified in the TS; and (4) test results satisfied acceptance

criteria

or were properly dispositioned.

The inspectors observed

all or portions of the following surveillances:

'

STP P-CSP-12, Revision 3, Routine Surveillance Test of Containment Spray

Pump 1-2"

-9-

STP V-313B, Revision 9, Full Stroke Exercise of Containment Spray Valve

CS-9001 B

STP P-RHR-11, Revision 4, Routine Surveillance Test of RHR Pump 1-1

b.

Observations

and Findin s

The inspectors found that the surveillances were scheduled

and performed at the

required frequency.

The procedures governing the surveillance tests were

technically adequate,

and personnel performing the surveillance demonstrated

an

adequate

level of knowledge.

The inspectors also noted that test results were

appropriately dispositioned.

M1.2.1

Solid State Protection S stem

SSPS

Train A Slave Rela

K645 Test

Unit 1

a.

Ins ection Sco

e 61726

The inspector observed the performance of STP M-16HA1, Revision 0, "Slave Relay

Test for Operation of Interposing Relay for Containment Spray Pump 2 (K645AX)."

The surveillance satisfies, in part, the licensee's commitment to test slave relays on

a quarterly basis.

b.

Observations

and Findin s

During performance of STP M-16AH1, SSPS test Reset Switch S821 stuck in the

test position and did not spring return to normal as required by procedure.

The

operator, with the concurrence of the senior control operator, manually repositioned

the switch to normal.

Switch S821 is in a test circuit for testing a portion of the

SSPS circuitry and is only utilized during testing and, therefore, does not affect the

operability of the SSPS.

Operators were able to complete the test and restore the

system to normal by the operator manually repositioning the switch. Subsequently,

the day following the completion of the surveillance, the inspector noted that the

operators had not documented the test reset switch deficiency on an AR. After the

inspector brought this to the attention of the licensee,

an AR was written.

c.

Conclusions

The failure to write an AR is a violation of OM7.ID1, "Problem Identification and

Resolution - Action Requests."

This failure constitutes

a violation of minor

significance and is being treated as a noncited violation consistent with Section IV

of the NRC Enforcement Policy (NCV 50-275/96021-02).

M1.2.2 Containment Pressure

Vacuum Relief Penetration Leakrate Test

a.

Ins ection Sco

e 61726

The inspector observed engineering personnel perform Surveillance Procedure

,l

t

-1 0-

STP V-663, "Penetration 63 Containment Isolation Valve Leak Testing," for the

Unit 1 containment pressure

and vacuum relief penetration.

Observations

and Findin s

The test personnel were knowledgeable of the test requirements

and were

observed briefing onshift operators prior to starting the test.

They used the

current revision of the procedure which had been issued for use that

morning. The procedure was performed as written with no difficulties. The

Portable Leak Test Monitor was within its required calibration frequency.

The results of the test were well within the established

acceptance

criteria

and consistent with the results of previous test results on the same

penetration.

The inspectors noted a problem involving Surveillance Procedure

STP V-663.

Procedure STP V-663 referenced TS 4.6.1.2.d as the applicable TS which

requires that containment isolation valves be tested with gas at P, of

47 psig. Technical Specification 4.6.1.2.d was deleted by TS

Amendment 110, approved March 1, 1996. Amendment 110 implemented

the new Option B - Performance

Based Requirements, of 10 CFR Part 50,

Appendix J, which have been incorporated into the licensee's Containment

Leakage Rate Testing Program.

A review of this program indicated that the

test requirements for containment isolation valves had not changed and,

therefore, the correct test was performed even though the incorrect TS was

referenced

in the surveillance procedure.

The inspector reviewed the licensee's computer based TS tracking system

entry made following the venting of the containment.

The TS tracking sheet

for this surveillance was reviewed by the inspectors and was also found to

reference the deleted TS surveillance.

As required by the administrative procedure for TS change process, the

licensee had initiated actions to change both the TS tracking sheet and the

surveillance procedure.

The reviews of the surveillance procedure and TS

tracking sheet had failed to identify the need to change the TS reference.

The licensee has since revised the surveillance procedure and the TS tracking

sheet to reflect the present requirements.

c.

Conclusions

The leakage rate test was performed correctly and the test results were

within the acceptance

criteria of the test procedure.

The technical

requirements contained in the current TS and the Containment Leakage Rate

Testing Program were satisfied, therefore, the correct test was performed

and there was no safety consequence

as a result of the incorrect reference

to TS 4.6.1.2.d.

However, the failure to identify the need to correct the TS

-11-

tracking sheet and surveillance procedure

is indicative of inattention to detail

during the review process.

M1.2.3 Main Steam Flow Instrumentation Surveillance

a.

Ins ection Sco

e 71707 61726

During control room observations, the inspectors observed the main control

board instrumentation and recorder traces for differences between channels

monitoring the same parameter

in order to detect inoperable channels.

b.

Observations

and Findin s

The inspector noted that the Unit 1 Loop 3 main steam flow indication in the

control room read approximately 10 percent less than the feedwater flow for

the same steam generator.

The steam flow and feedwater flow indications

on the other loops for both Units

1 and 2 were in close agreement.

The licensee investigated and determined the steam flow instrumentation had

not been normalized to the feedwater flow following the most recent plant

startup.

The normalization had previously been performed with the steam

flow/feedwater flow mismatch setpoint calibration performed in Surveillance

Procedure STP-42.

This setpoint had been deleted from the procedure as

part of the "Eagle 21" modification to the reactor protection system, and the

normalization of steam flow was not relocated to another procedure.

The licensee performed a POA and determined the low steam flow indication

had no impact on any safety system or safety function. These channels

provide indication and alarms only, and the normalization of the steam flow

instrumentation is desirable to provide useful indication to the operator.

The

steam flow indications are used by the operators in their abnormal operating

procedure for a loss of main feedwater pump.

Instrumentation in the Eagle

21 reactor protection system provides the input to accomplish the required

safety furictions and provide a redundant source of indication and alarms.

The licensee is preparing a procedure and plans to normalize all steam flow

instrumentation channels.

The inspectors reviewed the operability

assessment

and found it to be satisfactory and the proposed corrective

actions to be appropriate.

C.

Conclusions

The inappropriate deletion of requirements to normalize the steam flow

instrumentation is considered

a weakness

in the licensee's

procedure review and

revision process.

K ~ g

~

-1 2-

Miscellaneous Maintenance Issues (92902)

'8.

1

Closed

URI 50-275 96016-07: failure to set MSSVs in accordance with TS

requirements.

Following the dual reactor trip on August 10, 1996, three MSSVs,

two on Unit 2 (RV-4 and RV-8) and one on Unit 1 (RV-7), lifted below the lift

pressure at which they were thought to have been set.

Operators responded

by

adjusting the setpoint for the 10 percent atmospheric steam dumps to lower steam

generator

(SG) pressure to reseat the MSSVs.

These actions were not specifically

covered by procedure, but were considered to be prudent and warranted in order to

limitthe transient following the dual unit trip. The premature lifting of MSSVs did

not result in excessive cooldown.

MSSV Testin

Prior to the dual unit trip, maintenance

personnel had completed surveillance testing

of Unit 1 Lead

1 MSSVs using an hydraulic assist test device manufactured by AVK

Industries.

The testing was conducted in accordance with Maintenance Procedure

M-4.18, Revision 14, "Verification of Lift Point Using Ultra Star Assist Devise for

MSSVs." The TS requires that MSSVs set at 1065 psig must be set within -2

percent to + 3 percent of the nominal liftsetting and that MSSVs set at 1078,

1090, 1103, and 1115 psig be set within k3 percent of the liftsetting.

In

addition, the TS requires that the MSSVs be reset to within a 1 percent of their

specified liftsetting following main steam line code safety valve testing.

During

review of the MSSV test data the licensee identified that maintenance

personnel

had inadvertently utilized Unit 2 Lead

1 MSSV correction factors when testing Unit

1 Lead

1 MSSVs.

Use of the wrong correction factors resulted in the "as-left"

setting for three of the five valves being greater than +/-1 percent of the liftsetting

specified.

The licensee subsequently conducted MSSV surveillance testing on all MSSVs for

both Units

1 and 2 to ensure they were set to the TS required liftsettings. This

testing was conducted using Trevitest equipment in place of the AVK Ultra Star test

equipment.

Test results indicated that although the three Unit 1 Lead

1 MSSVs had

not been within the +/-1 percent of the required liftpressure, they were set close

enough to the liftsetpoints to preclude being outside of design basis.

After further

review, the licensee concluded, in Nonconformance Report N0001327, that "the

use of valve specific correction factors has been determined to be inaccurate."

The

safety consequence

of the improperly set MSSVs was low since the correction

factors for most valves were less than

1 percent.

The licensee later verified by

testing that the liftsetpoints were not set far enough out of tolerance to cause any

of the associated

design basis analyses to be exceeded.

The licensee also reviewed past test results for testing conducted with AVKtest

equipment.

Past AVKtest results were adjusted in order to correct for the effect of

valve specific correction factors.

Based upon these adjusted test results, the

licensee determined that during testing conducted between September 1995 and

August 1996, there were 53 instances where an MSSV had been returned to

-1 3-

service following main steam line code safety valve testing without being set to

within +/-1 percent of the TS required liftpressure.

The licensee plans to revise

Licensee Event Report 323/96-007to report this information. The licensee's

use of

valve specific correction factors were found to have been based upon limited

testing, and, therefore, there was insufficient conclusive data to derive correction

factors using statistical analysis.

The inspectors reviewed a prior violation of TS 3.7.1.1 (refer to EA 96-180) which

identified that two MSSVs were returned to service following testing without being

reset to within +/-1 percent of the TS required liftpressure.

The inspectors noted

that the cause of the prior violation was different from that of the current violation.

The inspectors concluded that the corrective actions in response to the prior

violation could not have been expected to prevent the current violation. The failure

to set MSSV liftsettings within +/-1 percent of their liftsetpoint following main

steam line code safety valve testing is a violation of TS 3.7.1.1

~ This licensee-

identified and corrected violation is being treated as a Non-Cited Violation,

consistent with Section VII.B.1 of the NRC Enforcement Policy (NCV 50-

275/96021-03).

MSSV Lifts Followin

Se tember 1995 Unit 2 Reactor Tri

Review of similar events indicated that following a Unit 2 reactor trip on

September 26, 1995, four MSSVs (relief valves (Rvs) 3, 7, 8, and 11) lifted

prematurely.

Operator response to the event was similar to that following the

August 10, 1996, dual unit trip in that operators reduced steam pressure

using the

10 percent atmospheric steam dump valves.

Prior to the reactor trip, MSSV testing

was in progress.

RV-7 had been tested and the valve liftsetpoint was in the

process of being adjusted in that the locknut for the liftpressure adjustment had not

been fullytightened.

As a result, following the reactor trip, RV-7's liftsetpoint

locknut loosened due to vibration causing the liftpressure to decrease

until

operators gagged the valve.

The licensee attributed the premature lifts on the three

remaining MSSVs to low liftpoints.

Following the September 1995 event, the

licensee suspected that the AVKtest methodology was introducing a bias, and the

valves that lifted low had been set at the low end of their characteristic curve.

Prior

to restart of the unit, the licensee conducted AVKtesting of unit 2 MSSVs and

conducted multiple lifts following valve liftpressure adjustment to ensure that the

valves were accurately set.

During subsequent

testing conducted at a safety valve test facility, the licensee

noted that MSSV test results using AVKtest equipment varied from results obtained

during valve testing with live steam.

Based upon the differences, the licensee

developed valve-specific characteristic curves and correction factors.

Based on the September 1995 and August 1996 events involving early lifting

MSSVs, the licensee performed insitu tests to compare the AVKtest methodology

with the industry accepted Trevitest methodology.

Differences were observed for

~

~

-14-

some MSSVs between liftsetpoints determined with the AVKmethod versus the

Trevitest method.

The correction factors were later suspected

to be inaccurate and

to introduce additional uncertainty in the valve liftsetting.

The licensee

subsequently discontinued the use of correction factors and the AVK Ultra Star test

equipment and started performing testing using Trevitest equipment.

Verification of Maintenance

Rule Re uirements

The inspector reviewed the licensee's

program for implementation of the

maintenance

rule for MSSVs. The licensee had determined that the MSSVs were

within the scope of the maintenance

rule and had included them as a component of

the portion of the turbine steam supply system upstream of the main steam

isolation valves (hereafter referred to as turbine steam supply system).

The licensee

scoping of the function of the turbine steam supply system determined that the

MSSVs were required for the following functions:

1) limiting primary system

temperature

and acting to maintain the system temperature below safety limits to

ensure fuel integrity and limit exposure to plant workers; 2) removing heat from the

primary system and providing for auxiliary feedwater addition for station blackout

conditions; and 3) maintaining integrity of portions of the main steam system

necessary to prevent a sudden cooldown that would add large amounts of positive

reactivity and could result in a brief return to criticality following a reactor trip. The

licensee determined the third function to be risk significant, since its contribution to

the core damage frequency was greater than 0.5 percent.

The licensee established

performance criteria for turbine steam supply system

components that were required for the system to fulfillits functions.

For the

MSSVs, the performance criteria was less than two maintenance

preventable

functional failures (MPFFs) during a 24 month period.

During discussions with the

system engineer, an MSSV MPFF was defined as a failure that caused the turbine

steam supply system to be unable to perform its safety function.

In review of the past 36 months of MSSV test results, the licensee concluded that

there had been no MSSV MPFFs.

Test results that indicated the MSSVs were

outside of the +/-3 percent tolerance required by TS were not considered by the

licensee to be MPFFs.

Specifically, during Unit 1 MSSV testing conducted on

September

14, 1995, the licensee identified high lifts for MSSVs associated

with

SG 1-1 that placed the unit outside of design basis, since the "as-found" test

results indicated the potential during an accident for SG pressure to have exceeded

110 percent of design pressure.

The licensee evaluated this occurrence

as not

constituting an MPFF, since the SG would have remained intact and performed its

function of removing primary system heat.

This condition was reported by the

licensee in Licensee Event Report 275/95-011-00.

Since the licensee established

the threshold for an MSSV MPFF at the point where

the turbine steam supply system would no longer perform its safety function, the

use of MPFFs for MSSV performance trending was ineffective and did not provide a

-1 5-

true indication of component reliability. The system level performance criteria

resulted in too high a threshold for MSSV performance deficiencies.

Therefore, the

established

MSSV condition monitoring did not provide an appropriate basis for

determining satisfactory performance of the MSSVs to fulfilltheir intended safety

function. The failure to establish appropriate performance criteria for the MSSVs

that adequately demonstrated

effective maintenance

is a violation of 10 CFR 50.65

(VIO 50-275;323/96021-04).

During the review, it was noted that the licensee had initiallyplaced the MSSVs in

condition monitoring (i.e. Category A(2)); however, the reviews performed to

evaluate the turbine steam supply system for the past 36 months had not been

documented.

This action appeared to be in conflict with the guidance provided in

paragraph

13.2.1 of NUMARC 93-01 Revision 2, "Industry Guidelines for

Monitoring the Effectiveness of Maintenance at Nuclear Power Plants," which

specifies that the basis from the initial scoping for placing a structure, system or

component in Category A(2) should be documented.

Further investigation of this

issue, revealed that the licensee did not require formal documentation of the

reviews.

Actions Initiated b

the Licensee Followin

Dual Unit Tri

On August 29, 1996, the licensee's maintenance

rule expert panel met and, based

upon the MSSV performance problems, placed Units

1 and 2 MSSVs in goal setting

and monitoring (i.e. Category A(1)) until December 1997. The goal the licensee has

established for the valves is no TS violations due to improper or drifted setpoints.

Conclusions

The maintenance

rule program performance criteria established for MSSVs was

ineffective in detecting unsatisfactory MSSV performance.

The licensee's decision

to not require documenting the basis for initial scoping decisions is considered to be

a weakness

in the licensee's implementation of the maintenance

rule.

Due to

improper use of correction factors, MSSVs had not been reset to within +/-1

percent of the TS required liftsetpoint following main steam line code safety valve

testing prior to returning the valves to service.

Closed

IFI 50-275 323 91039-02: periodic verification of motor-operated valve

switch settings.

This item involved the licensee's motor-operated valve program, in

response to Generic Letter 89-10, specifically in the area of periodic verification of

motor-operated valve switch settings.

The licensee submitted additional information

in a letter dated May 5, 1995, as requested

in NRC Inspection

Report 50-275;323/95001.

This information was reviewed by the inspectors and

found to be adequate for closure of the licensee's

Generic Letter 89-10 program.

The licensee was notified of the results of this review in a letter dated August 3,

1995.

l

-1 6-

M8.3

Closed

IFI 50-275 96016-03'50-323

96016-03installation of improper

auxiliary saltwater (ASW) pump shaft key.

During refurbishment of an

ASW pump, the licensee discovered one of the pump shaft coupling keys

missing and, subsequently,

determined that a key, made of a material

different from that specified, had been installed and had dissolved in the

saltwater environment.

Following discovery of the problem, an inspection

followup item was created to assess

the licensee's evaluation of the ASW

pump's past operability and long term corrective actions.

The shaft appeared to have galled to the coupling, allowing the pump to

continue to operate and pass its surveillance tests.

The shaft coupling joint

was removed by cutting the upper and intermediate shafts a distance away

from the coupling to preserve the joint. The shaft coupling assembly was

then sent to a test laboratory for testing.

The testing subjected the coupling

to. torsional loads.

Based upon the results of the tests the licensee

determined the joint would not yield at less than the breakdown torque of

the ASW pump.

Therefore, since the seismic load to the joint is small, the

licensee concluded the pump would have remained functional during design

basis seismic events.

The proposed barriers and corrective actions include changing the descriptor

for the shaft key to clarify its proper use and the addition of a discussion of

this event to the outage maintenance

worker orientation training. Other

administrative changes that have occurred since the installation of the

improper key have sensitized maintenance

personnel to the need for "like for

like" replacements.

The inspector concluded the past operability evaluation

and long term corrective actions appeared to adequately address the issue.

III. Engineering

E1

Conduct of Engineering

E1.1

RHR S stem Review

a 0

Ins ection Sco

e 71707 37551

The inspectors conducted

a review of the design, maintenance,

and operation of the

RHR system which included its normal function of decay heat removal and its

emergency core cooling function.

The review included the following documents:

~

UFSAR: Chapter 5.5, Chapter 6.3, Chapter 15

~

DCM S-9, Safety Injection System

~

DCM S-10, Residual Heat Removal System

~

Il

,g(

-1 7-

~

Plant Technical Specifications

~

Design Change Packages:

~

EP-46408, Revision 1, Pipe Support Modification

~

EN-49118, Revision 0, Upgrade RHR Pump and Heat Exchanger Design

Pressure

EP-45955, Revision 0, Modify RHR Miniflow Check Valve Disc

EE-46046, Revision 0, Reset Time Delay for RHR Pump Low Flow Alarm

EM-44172, Revision 1, Install RHR Miniflow Check Valves

SJ-45237, Revision 0, Replace RHR Pump Motor Upper Bearing Oil

Sightglass

EE-41602, Revision 0, Replace Safety Injection Signal Timing Relays

EM-41490, Revision 0, Remove MELB Spray Guards on Seal Water Cooler

Lines

PGSE Calc. SQE-46, Seismic Evaluation of Replacement Motor for RHR

Pump

PGRE Calc. PG-1049, RHR System Cooldown Capacity

RHR Pump/Motor Vendor Manual

RHR System Operating Procedures

Procedure

EOP E-1.3, Transfer to Cold Leg Recirculation

PGSE RHR Safety System Functional Audit and Review, November 1993

The inspector also conducted

a detailed walkdown of the accessible

portions of the

RHR system and interviewed the system engineer.

Observations

and Findin s

The RHR system is a dual-purpose system in that it provides for core decay heat

removal during shutdown/refueling conditions and during accident conditions.

It

also provides a redundant means of coolant injection during the initial phase of a

large break LOCA. The bases under which the system is designed to perform these

functions are described

in the UFSAR and in DCMs S-9 and S-10.

~

~

LQ

-1 8-

The licensee's

procedure for transferring the'CCS from injection to recirculation

mode is described

in Table 6.3-4 of the UFSAR. The licensee's

EOP Implementing

Procedure,

E-1.3, Transfer to Cold Leg Recirculation, was noted to cont'ain several

deviations from that described

in UFSAR. This issue is more fully discussed

in

Section 01.2.

The engineers involved with the system were knowledgeable on system design and

operation, historical design issues and system changes,

and current system

deficiencies.

A detailed walkdown of the accessible

portions of the system found

only one deficiency that had not already been identified by the licensee

(a

yoke-to-bonnet dry boric acid leak on a system valve).

The system engineer agreed

that the deficiency should be evaluated during routine system walkdowns and

considered including the valve in the RHR system tracking AR for dry boric acid

leaks.

During the inspection period, the system engineer identified that the upper motor

bearing on RHR Pump 1-1 had increased

oil consumption.

The system engineer had

been tracking the oil consumption through an AR. The system engineer evaluated

the increased consumption and determined that the pump may not have been able

to perform its function over the entire postaccident

period for which it would be

required.

Consequently, the engineer recommended that operations declare the

pump inoperable while repairs to the upper bearing sight glass, the source of the oil

leak, were effected.

This demonstrated

appropriate monitoring of equipment

performance and sensitivity to the impact of equipment deficiencies on the ability of

a component to perform its design basis function.

A discrepancy was noted between the UFSAR and DCM S-10 with regard to the

design cooldown capability of the RHR system.

Section 4.3.1 of DCM S-10 states

that the RHR system is capable of cooling the RCS from 350

F to 140

F within

10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> based upon two trains operating at design flow and RHR initiated 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />

after reactor shutdown.

Additionally, the DCM states that valve interlocks prevent

initiation of RHR until RCS pressure

is less than approximately 390 psig.

Section 5.5.6.1 of the UFSAR states that the RHR system is designed to perform

the same function within 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br /> and at an initial pressure

less than 425 psig.

These design parameters

are also provided in Table 5.5-8 of the UFSAR. It was

noted that the licensee's initiative to review and update the FSAR, which was

completed and scheduled to be submitted in November 1996, also identified these

discrepancies

and has revised Section 5.5.6.1 to be consistent with the DCM.

However, Table 5.5-8 in the FSAR update had not been revised to reflect the DCM

values.

The inspector reviewed PGSE calculation SQE-46 for qualification of the RHR pump

replacement motor to be installed with RHR Pump 1-1. The evaluation concluded

that the replacement motor was acceptable with the limitation that the material of

motor holddown bolts be ASTM A-193, Grade B7, and that they be torqued to

124 ft-lb. Adequate documentation could not be found in the work package

~

~

-19-

associated

with the motor's installation to determine that these limitations were

implemented.

An inspection followup item is being initiated to track resolution on

the actual torque applied to the RHR Pump 1-1 motor holddown bolts and its

consistency with the motor's seismic qualification evaluation

(IFI 50-275/96021-05).

C.

Conclusions

Several discrepancies

were identified in FSAR update with regard to the RHR

system design parameters.

These discrepancies

illustrated a weakness

in the

licensee's program to update the FSAR to reflect current design and operation of

the plant.

System engineering for the RHR system was considered strong.

This was

supported by both the knowledge of the system engineer and the active role the

engineer has played in identifying, tracking, and correcting system deficiencies.

E1.2

ASW S stem Review

a ~

Ins ection Sco

e 71707 37551

The inspectors reviewed documentation related to the ASW system,

including:

UFSAR Section 9.2.7 Auxiliary Saltwater System

~

System Engineer Quarterly Reports

Ars: A02217,50, A0275649, A0312240, A0330165,

A0344300,A0365445,A0366935,A0374286,A0390005,

A0397706,A0399769,A0400931,A0401616,A0401949,

A0403369,A0404763,A0410203

~

Nonconformance Reports N0001814 and N0001992

~

PSRC TS Interpretation 95-08, Revision

1

~

Operability Evaluation 95-11, Operability of Component

Cooling Water System (CCW) with Analyzed CCW Water

Temperatures

Higher Than Current Design Basis

~

EOP E-0 Reactor Trip or Safety Injection, and E-1.3 Transfer to

Cold Leg Recirculation

The inspectors walked down portions of the system in both Units

1 and 2

and observed equipment operation, valve alignments and seals, AR tags and

overall material condition of the equipment.

'0

-20-

Observations

and Findin s

ASW S stem Walkdown

A walkdown of portions of the system was performed for both Units

1 and 2

and found the valve alignment to be correct and seals installed on specified

valves.

The oil levels for the pumps were within their required bands.

The

operating pumps had adequate

seal leakoff flow and the room coolers were

in service.

The system instrumentation was indicating properly.

The backup

air bottles were properly pressurized

and aligned to the heat exchanger inlet

isolation valves.

The overall material condition of the equipment was good

with few open AR tags noted.

ASW TS Re uirements

The TS Limiting Condition for Operation 3.7.4.1, requires at least two ASW

trains shall be OPERABLE, with an ACTION statement that with only one

ASW train OPERABLE, restore at least two trains to OPERABLE status within

72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or be in at least HOT STANDBYwithin the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in

COLD SHUTDOWN within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.

The PSRC has interpreted that to comply with the ACTION statement the

following conditions must exist: 1) two ASW pumps and one CCW heat

exchanger,

or 2) one ASW pump and two CCW heat exchangers,

or 3) one

train (ASW pump and CCW heat exchanger) with the capability to restore at

least one additional ASW pump or CCW heat exchanger within 20 minutes of

receipt of an Sl, or 4) one train (ASW pump and CCW heat exchanger) with

an engineering evaluation for single train operation without the restriction of

Item 3 above.

The interpretation resulted from an RHR heat exchanger test which predicted

overheating of CCW during the cold leg recirculation phase following a

LOCA, under certain limiting conditions of a single train failure and most

conservative fouling factors in the RHR heat exchanger,

CCW heat

exchanger and CFCUs.

The additional requirements

in the TS interpretation

ensure that adequate

equipment is available to prevent overheating the

CCW.

The inspectors reviewed and verified that the EOPs contained the appropriate

directions to satisfy the additional restrictions of this interpretation.

The licensee agreed with the inspector's conclusion that this TS

interpretation was not consistent with the UFSAR, which describes the ASW

system as comprised of fully redundant active components, with two 100

percent capacity pumps, with piping system arranged to provide two

separate,

redundant supply headers,

either of which can supply the minimum

required flow for ESF operation, and each pump sized to provide water for

(

w

Q)

-21-

one CCW heat exchanger.

Subsequent to the end of the inspection period,

the licensee revised the UFSAR to be consistent with the TS interpretation.

The inspectors plan to review the licensee's

10 CFR 50.59 evaluation of this

change.

The conditions which resulted in this TS interpretation imply that the Limiting

Condition for Operation and its ACTION statement do not define the lowest

functional capability or performance levels for the ASW system.

Therefore,

the potential need for a TS amendment has been questioned by the

inspectors.

This issue and the inspectors'eview of the licensee's

10 CFR 50.59 evaluation remain an unresolved item (URI 50-275;323/

96021-06).

C.

Conclusions

The ASW system was found in proper configuration to support its safety

function, and overall material condition of the equipment was satisfactory.

E8

IVliscellaneous Engineering Issues (92903)

E8.1

Closed

IFI 50-275 323 96020-02: PSRC interpretation of TS 3.4.6.2.e. allowed

for controlled leakage measured

at 2235 a 20 psig to slightly exceed 40 gpm.

The

inspectors questioned the validity of this TS interpretation since it appeared to be in

conflict with the TS specified limit of 40 gpm for controlled leakage.

The licensee

provided information that although the surveillance allowed for the controlled

leakage to exceed 40 gpm that the measured controlled leakage had never

exceeded the 40 gpm value.

'he

TS requires that controlled leakage be measured

at least once every 31 days at

nominal RCS pressure of 2235 psig with the modulating valve fully open.

This

limitation ensures that in the event of a LOCA, the safety injection flow willnot be

less than that assumed

in the safety analysis.

The PSRC's basis for allowing

controlled leakage to exceed 40 gpm at 2235 psig was that the corresponding

calculated total leakage during the safety injection phase would be (40 gpm.

The

licensee's

surveillance procedure for measuring controlled leakage calculated the

total line resistance

of the reactor coolant pump (RCP) seal injection lines, and

verified through calculation, that the flow resistance was above a specified value in

order to ensure,

in the event of a LOCA, that the controlled leakage would not

exceed the TS limit. The inspectors reviewed STP M-54, Revision 18, "Verification

of RCP Seal Injection Flow by Resistance

Measurement,"

and concluded that the

licensee's method of calculating the RCP seal injection line flow resistance,

and

then utilizing that resistance to calculate controlled leakage, was an acceptable

method for ensuring the TS requirement was met.

However, PSRC TS

interpretation 96-08 and STP M-54, which both allowed measured,

controlled

leakage to be in excess of the limit specified in TS 3.4.6.2.e., did not appear to be

acceptable to the inspectors.

~

r

J

~

-22-

Based upon the concern for compliance with the TS as written, the licensee revised

STP M-54 to no longer accept measured,

controlled leakage in excess of 40 gpm.

Additionally, the PSRC rescinded TS interpretation 96-08.

The inspector concluded that the PSRC had inappropriately approved

a TS

interpretation which, although meeting the intent of the TS, allowed a condition that

appeared different from the TS wording.

Since the licensee has reinstated the

40 gpm limit, this item is closed.

E8.2

Closed

IFI 50-275 323 93019-02:pressure

locking and thermal binding of motor-

operated valves.

This item involved the licensee's efforts to complete reviews of its

Generic Letter 89-10 motor-operated valve population for susceptibility to pressure

locking and thermal binding and 'to take corrective actions, where necessary,

to

ensure valve operability.

Subsequently, the NRC issued Generic Letter 95-07,

"Pressure Locking and Thermal Binding of Safety-Related Power-Operated

Gate

Valves." The licensee's

response to this generic letter is currently under review by

the NRC Office of Nuclear Reactor Regulation.

This issue will be fully resolved

under Generic Letter 95-07; therefore, this item has been closed.

IV. Plant Su

ort

V. Mana ement IVleetin s

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management

at the

conclusion of the inspection on November 8, 1996.

The licensee acknowledged the

findings presented.

The inspectors asked the licensee whether any materials examined during the inspection

should be considered proprietary.

No proprietary information was identified.

0

ATTACHMENT

SUPPLEMENTAL INFORMATION

PARTIALLIST OF PERSONS CONTACTED

Licensee

S. D. Allen, Supervisor, Mechanical Engineering Valve Group

T. R. Baldwin, Supervisor, ECCS Systems

J. R. Becker, Director, Operations

K. H. Bych, Director, Nuclear Quality Services

'. F. Fetterman, Director, Instrumentation and Control Engineering

L. L. Fusco, Engineer, Predictive Maintenance

T. L. Grebel, Director, Regulatory Services

C. D. Harbor, Supervisor, Regulatory Services

T. L. McKnight, Engineer, Regulatory Services

D. B. Miklush, Manager, Engineering Services

J. E. Molden, Manager, Operations Services

M. N. Norem, Director, Mechanical Maintenance

D. A. Vosburg, Director, Nuclear Steam Supply Systems Engineering

L. F. Womack, Vice President,

Nuclear Technical Services

INSPECTION PROCEDURES USED

IP 37551: Onsite Engineering

IP 61726: Surveillance Observations

IP 62707: Maintenance Observations

IP 71707: Plant Operations

IP 71750: Plant Support

IP 92901: Followup - Plant Operations

IP 92902: Followup - Maintenance

IP 92903: Followup - Engineering

ITEMS OPENED

CLOSED AND DISCUSSED

~Oened

50-275;323/96021-01

50-275/96021-02

50-275;323/96021-03

50-275;323/96021-04

50-275/96021-05

50-275;323/96021-06

EEI

failure to perform 10 CFR Part 50.59 evaluation when

revising EOP E-1.3

NCV

failure to document an equipment problem

NCV

failure to set MSSVs within a1'/0 of TS liftsetpoint

NOV

establishment of inadequate

performance criteria

IFI

RHR pump 1-1 motor hold down bolt torque

URI

ASW TS interpretation

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Closed

50-275;323/9601 6-03

IF I

50-275/9601 6-07

URI

50-275;323/96020-02

50-275;323/9301 9-02

IFI

IFI

50-323/9501 8-02

VIO

50-275;323/91 039-02

IFI

improper shaft key utilized for assembly of ASW pump

shaft

failure to set MSSVs in accordance with TS

requirements

periodic verification of motor-operated valve switch

settings

PSRC interpretation of TS 3.4.6.2.e

pressure locking and thermal binding of motor-operated

valves

reactor cavity sump level indication and recorder

LIST OF ACRONYMS USED

AR

ASTM

ASW

CCP

CCW

ECCS

EOP

IFI

LCO

LOCA

MPFF

MSSV

OP

PG&E

POA

PDR

PSRC

RCP

RCS

RHR

RV

RWST

SG

SSC

SSPS

STP

TS

UFSAR

URI

action request

American Society of Testing and Measurement

auxiliary saltwater

centrifugal charging pump

component cooling water

emergency core cooling system

emergency operating procedure

inspection followup item

limiting condition of operation

loss of coolant accident

maintenance

preventable functional failure

main steam safety valve

operating procedure

.Pacific Gas and Electric

prompt operability assessment

public document room

plant staff review committee

reactor coolant pump

reactor coolant system

residual heat removal

relief valve

refueling water storage tank

steam generator

structures, systems or components

solid state protection system

surveillance test procedure

Technical Specification

Updated Final Safety Analysis Report

unresolved item

I

0

ENCLOSURE 3

V. PREDECISIONAL ENFORCEIVIENT CONFERENCES

Whenever the NRC has learned of the existence of 'a potential violation for which escalated

enforcement action appears to be warranted, or recurring nonconformance

on the part of a

vendor, the NRC may provide an opportunity for a predecisional enforcement conference

with the licensee, vendor, or other person before taking enforcement action.

The purpose

of the conference

is to obtain information that willassist the NRC in determining the

appropriate enforcement action, sucn as: (1) a common understanding of facts, root

causes

and missed opportunities associated

with the apparent violations, (2) a common

understanding of corrective action taken or planned, and (3) a common understanding of

the significance of issues and the need for lasting comprehensive

corrective action.

If the NRC concludes that it has sufficient information to make an informed

enforcement decision,

a conference will not normally be held unless the licensee requests

it. However, an opportunity for a conference willnormally be provided before issuing an

order based on a violation of the rule on Deliberate Misconduct or a'civil penalty to an

unlicensed person.

If a conference

is not held, the licensee will normally be requested to

provide a written response to an inspection report, if issued, as to the licensee's views on

the apparent violations and their root causes

and a description of planned or implemented

corrective action.

During the predecisional enforcement conference, the licensee, vendor, or other

persons will be given an opportunity to provide information consistent with the purpose of

the conference,

including an explanation to the NRC of the immediate corrective actions (if

any) that were taken following identification of the potential violation or nonconformance

and the long-term comprehensive

actions that were taken or will be taken to prevent

recurrence.

Licensees,

vendors, or other persons will be told when a meeting is a

predecisional enforcement conference.

A predecisional enforcement conference

is a meeting between the NRC and the

licensee.

Conferences

are normally held in the regional offices and are not normally open

to public observation.

However, a trial program is being conducted to open approximately

25 percent of all eligible conferences for public observation, i.e., every fourth eligible

conference involving one of three categories of licensees

(reactor, hospital, and other

materials licensees) will be open to the public. Conferences will not normally be open to

the public if the enforcement action being contemplated:

(1) Would be taken against an individual, or if the action, though not taken against

an individual, turns on whether an individual has committed wrongdoing;

(2) Involves significant personnel failures where the NRC has requested that the

individual(s) involved be present at the conference;

(3) Is based on the findings of an NRC Office of Investigations

report; or

(4) Involves safeguards

information, Privacy Act information, or information which

could be considered proprietary;

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In addition, conferences will not normally be'pen to the public if:

(5) The conference involves medical misadministrations or overexposures

and the

conference cannot be conducted without disclosing the exposed individual's name; or

(6) The conference will be conducted by telephone or the conference will be

conducted at a relatively small licensee's facility.

Notwithstanding meeting any of these criteria, a conference may still be open if the

conference involves issues related to an ongoing adjudicatory proceeding with one or more

intervenors or where the evidentiary basis for the conference

is a matter of public record,

such as an adjudicatory decision by the Department of Labor.

In addition, with the

approval of the Executive Director for Operations, conferences willnot be open to the

public where good cause has been shown after balancing the benefit of the public

observation against the potential impact on the agency's enforcement action in a particular

case.

As soon as it is determined that a conference will be open to public observation, the

NRC willnotify the licensee that the conference will be open to public observation as part

of the agency's trial program.

Consistent with the agency's policy on open meetings,

"Staff Meetings Open to Public," published September 20, 1994 (59 FR 48340), the NRC

intends to announce open conferences

normally at least 10 working days in advance of

conferences through (1) notices posted in the Public Document Room, (2) a toll-free

telephone recording at 800-952-9674,and

(3) a toll-free electronic bulletin board at 800-

952-9676.

In addition, the NRC will also issue

a press release and notify appropriate State

liaison officers that a predecisional enforcement conference

has been scheduled

and that it

is open to public observation.

The public attending open conferences

under the trial program may observe but not

participate in the conference.

It is noted that the purpose of conducting open conferences

. under the trial program is not to maximize public attendance,

but rather to determine

whether providing the public with opportunities to be informed of NRC activities is

compatible with the NRC's ability to exercise its regulatory and safety responsibilities.

Therefore, members of the public will be allowed access to the NRC regional offices to

attend open enforcement conferences

in accordance with the "Standard Operating

Procedures

For Providing Security Support For NRC Hearings And Meetings," published

November 1, 1991 (56 FR 56251).

These procedures

provide that visitors may be subject

to personnel screening, that signs, banners, posters, etc., not larger than 18" be permitted,

and that disruptive persons may be removed.

Members of the public attending open conferences will be reminded that (1) the

apparent violations discussed

at predecisional enforcement conferences

are subject to

further review and may be subject to change prior to any resulting enforcement action and

(2) the statements

of views or expressions of opinion made by NRC employees at

predecisional enforcement conferences,

or the lack thereof, are not intended to represent

final determinations or beliefs.

Persons attending open conferences will be provided an

opportunity to submit written comments concerning the trial program anonymously to the

I

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regional office. These comments will be subsequently forwarded to the Director of the

Office of Enforcement for review and consideration.

When needed to protect the public health and safety or common defense

and

security, escalated

enforcement action, such as the issuance of an immediately effective

order, will be taken before the conference.

In these cases,

a conference may be held after

the escalated enforcement action is taken.

t