ML16342D729

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Insp Repts 50-275/97-06 & 50-323/97-06 on 970427-0607. Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support
ML16342D729
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 07/09/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML16342D728 List:
References
50-275-97-06, 50-275-97-6, 50-323-97-06, 50-323-97-6, NUDOCS 9707110200
Download: ML16342D729 (74)


See also: IR 05000275/1997006

Text

ENCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket Nos.:

License Nos.:

Report No.:

Licensee:

Facility:

Location:

Dates:

Inspectors:

50-275

50-323

DPR-80

DPR-82

50-275/97006

50-323/97006

Pacific Gas and Electric Company

Diablo Canyon Nuclear Power Plant, Units

1 and 2

7 1/2 miles NW of Avila Beach

Avila Beach, California

April 27 through June 7, 1997

M. Tschiltz, Senior Resident Inspector

D. Allen, Resident Inspector

R. Huey, Technical Assistant, Walnut Creek Field Office

J. Kramer, Resident Inspector, San Onofre

S. Boynton, Resident Inspector

Approved By:

H. Wong, Chief, Reactor Projects Branch

E

ATTACHMENT:

Supplemental

Information

9707ii0200 970709

PDR

ADQCK 05000275

6

PDR

EXECUTIVE SUMMARY

Diablo Canyon Nuclear Power Plant, Units

1 and 2

NRC Inspection Report 50-275/97-06; 50-323/97-06

~Oerations

Operators were not observant to tagging discrepancies

identified by the inspectors

and when brought to the licensee's

attention personnel failed to initiate trending

records.

This was not in keeping with operations management

expectations

(Section 01.1).

A violation was identified when, for a brief time (3 minutes) in Unit 2, a licensed

reactor operator was not present

in the operator-at-the-controls

area.

Informal

communications

resulted in the relief operator not assuming the at-the-controls

duties for the Unit 2 control operator (Section 01.2).

Operators responding to a Steam Generator

(SG) 1-3 nozzle dam alarm took

approximately 30 minutes to enter containment to investigate and correct the cause

of the alarm.

This response

was considered

untimely and was determined not to be

in accordance

with management

expectations

(Section 01.3).

Preparations

for reducing the reactor coolant system inventory to mid-loop to

facilitate removal of SG nozzle dams were thorough.

Operators were provided with

time to review and discuss the applicable procedures

prior to performance.

Control

room activities were reduced to limit the potential for distraction and appropriate

attention was given to the evolution by Operations management

(Section 01.4).

The inspectors identified a violation when three of the four seismic restraining bolts

on the breaker cubicle for Safety Injection (Sl) Pump 2-2 were found not to be

properly installed as specified in procedures.

This condition was different than the

seismic analysis for breaker qualification.

Inadequately tightened bolts had been

a

problem found by inspectors

in the past.

Subsequent

analysis showed that the

breaker remained operable with the loose fasteners

(Section 01.5).

~

The Operations shift supervisor and shift foreman demonstrated

good command and

control during preparations for return-to-power operation at the end of Refueling

Outage 1R8.

Operator peer checking was consistently implemented

and was

effective in identifying and correcting minor problems before they occurred

(Section 01.8).

~

Operator training on major changes to the equipment clearance

process prior to

Refueling Outage

1R8 did not appear to have fully covered all appropriate aspects of

new responsibilities for each individual involved in the new process.

Also,

additional training on the bases for significant clearance

process changes

appeared

warranted (Section 01.8).

-2-

Maintenance

~

Outage scheduling

and planning were accomplished with a specific emphasis

on

safety and maintaining equipment operable

or available as required by the outage

safety plan.

Communications

between organizations

regarding changes

in the

schedule

appropriately addressed

changes

in the outage safety plan. The outage

safety plan and schedule were clearly communicated to the organization in meetings

and daily status reports that were published and distributed to workers

(Section M6.1).

For the maintenance. activities observed,

both technical maintenance

and

mechanical maintenance

personnel

were knowledgeable

of the assigned

tasks.

Appropriate authorization had been obtained for the work and the work package

instructions were closely followed (Section M1.1).

A non-cited violation was identified when the licensee noted that residual heat

removal (RHR) and excess letdown heat exchanger

seismic supports surveillances

were not performed as required by Technical Specification (TS) 4.05 and Section XI

of the ASME code (Section M8.1).

A non-cited violation was identified when the licensee found that procedures

failed

to provide adequate

instructions for installation of the power supply to the

containment source range audio count rate/scalcr timer. As a result, after

unintentionally de-energizing the power source to the sealer timer, the TS required

continuous audible count indication was not available in containment for

approximately

1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> during core alterations (Section 08.1).

Nuclear Quality Services (NQS) assessments

of performance

during Refueling

Outage

1R8 were effective in identifying performance

problems to plant

management.

Assessments

were issued in a timely manner and provided

management

with the information needed to focus attention on problem areas

(Section M7.1).

Encnineering

A violation was identified involving the spray shields for the reactor coolant

pump (RCP) oil collection system,

Although the licensee determined that

inspections

should be performed in response

to Information Notice (IN) 94-58, no

inspections of the Unit 1 RCP oil collection system had been performed.

There had

been several opportunities to do so and, in addition, an assessment

of Unit 2 did

not identify the spray shield discrepancy

(Section E1.1).

A non-cited violation was identified when a Quality Assurance

engineer alerted

cognizant system engineers that an action request

(AR) that identified the need to

test main feed pump (MFP) turbine stop valves had incorrectly been closed without

initiating actions to accomplish the testing.

This demonstrated

competerice

in the

-3-

NQS organization, but was also indicative of a lack of appropriate follow through

and review of corrective actions within the Engineering organization (Section E8.1).

~

During reviews of the licensee's

disposition of Updated Final Safety Analysis

Report (UFSAR) discrepancies,

the inspector determined that changes to the Final

Safety Analysis Report (FSAR) had been included in Revision 11 without the

required safety evaluations

(Section E8.2).

Plant Su

ort

~

Operations personnel failed to establish adequate

controls to ensure Valve SFS-50

remained closed during hydrolasing of the lower reactor cavity. As a result, due to

the combination of an incorrect status board and inadequate

verification of

Valve SFS-50 valve position, hydrolasing was conducted with the valve open,

which resulted in the spread of contamination into the fuel handling building (FHB)

(Section

R1

~ 1).

Re ort Details

Summar

of Plant Status

Unit

1 began this inspection period in Mode 6 (performing fuel offload) for the unit's eighth

refueling outage

(1RS).

The unit entered Mode

1 on June

1, 1997,

and returned to

100 percent power on June 7.

Unit 2 began this inspection period at 100 percent power.

On June

1, power was reduced

to 75 percent to perform turbine stop valve testing and maintenance

on the MFP 2-1 speed

control system.

Subsequently,

the unit power was reduced to 50 percent to perform

additional MFP stop valve testing.

Unit 2 returned to 100 percent power on June

1 and

operated

at that level for the remainder of the inspection period.

I. 0 erations

01

Conduct of Operations

01.1

General Comments

71707

Using Inspection Procedure 71707, the inspectors conducted frequent reviews of

ongoing plant operations.

In general, the conduct of operations was professional

and safety conscious.

The Senior Resident Inspector and Reactor Projects Branch

Chief conducted

a review of the Institute of Nuclear Power Operations evaluation

completed during this inspection period (conducted

March 3-10, 1997).

The

Institute of Nuclear Power Operations results were consistent with NRC's views of

licensee performance.

No additional followup actions are considered warranted.

Control room activities during the 1RS outage appeared to be well coordinated

and

controlled.

The inspector noted that the additional licensed operators put in the

control room for the outage allowed the control room.workload to be more evenly

distributed among the operators.

In particular, the addition of a second shift

supervisor,

a shift foreman's assistant,

and an additional reactor operator was seen

as a significant commitment by licensee management

to better manage outage

activities.

During the inspection period, inspectors noted several instances where caution tag

stickers were incorrectly placed on the Unit 1 control room control panels, and an

AR sticker that was left on the control board after the AR had been closed.

After

the inspector pointed out the discrepancies,

the caution tag stickers were moved to

the correct components

and the AR sticker was removed; however, the

discrepancies

were not documented.

After discussion with the operations director,

the inspector noted that it was management's

expectation that these types of

performance

errors be documented

by writing event trend. records.

After the

inspector discussed this with the operations director, these discrepancies

were

documented.

0

-2-

01.2

Failure to Maintain an 0 erator-at-the-Controls

at all Times

Ins ection Sco

e 71707

The inspectors reviewed an incident in which the licensee identified that the Unit 1

senior control operator (SCO) left the control room after assuming the duties of the

Unit 2 operator-at-the-controls.

At the time, Unit 2 was at 100 percent power.

As

a result, there was no one assigned

to monitor Unit 2 control room indications and

alarms for a period of approximately 3 minutes.

The following documents

were

reviewed:

~

AR A0435466, Violation of Procedure

OP1.DC12

~

Procedure

OP1.DC12, "Conduct of Routine Operations"

b.

Observations

and Findin

s

In reviewing this occurrence,

the inspector discussed

the sequence

of events with

the shift foreman (SFM) on duty for Unit 2 during this time.

The situation arose

when the Unit 2 control operator (CO) sought

a relief to allow him to leave the

"operator-at-the-controls"

area to go to the rest room.

The rest room, although

within the control room envelo'pe,

is outside of that area in which an operator-at-

the-controls is required to be stationed at all times.

At the time, the Unit 2 SCO was in containment performing a routine inspection and

the balance of plant CO, who is also a licensed reactor operator, was out of the

control room performing rounds.

As a result, the Unit 2 CO requested

relief and

was relieved by the Unit 1 SCO.

As provided by licensee procedures,

no formal

turnover is required for reliefs of this nature.

The Unit

1 SCO was on the phone

when the Unit 2 CO requested

the relief. Although the Unit 1 SCO apparently

acknowledged

the request,

he later left the control room after assuming the duties

of operator-at-the-controls.

Approximately 3 minutes later, when the Unit 2 SFM

stood up from his desk, he noted that there was not a licensed operator in the

designated

operator-at-the-controls

area.

At that point, the SFM assumed

the

operator-at-the-control

duties until another licensed operator was summoned to

assume the operator-at-the-controls

position.

The operations director noted that during the time there was no licensed operator

assigned

as the operator-at-the-controls,

the SFM was at his desk on the edge of

the operator-at-the-controls

area as defined in Attachment 7.5 of

Procedure

OP1.DC12.

The SFM was located where he would have heard and been

able to respond to control room annunciators.

In reviewing the information provided

by the licensee, the inspector determined that it was reasonable

to conclude that

the SFM was knowledgeable

of plant conditions and work in progress

and that he

was positioned in a way that he would have heard and responded

to any control

board al'arms,

It should also be noted that during this same time period there were

-3-

more than the TS minimum number of licensed senior reactor operators

and reactor

operators

in the control room.

Procedure

OP1.DC12, Section 5.11.3, allows the operator-at-the-controls

to enter

other areas within the control room envelope outside of that designated

as the

"operator-at-the-controls"

area provided the SCO or another cognizant licensed

operator is stationed such that he is attentive to control room indications and

alarms.

Procedure

OP1.DC12 also notes the operator preferably would be

positioned at the CO's desk or in front of the vertical boards.

TS 6.8.1 states,

in

part, that written procedures

shall be established,

implemented and maintained

covering the applicable procedures

in Appendix A of Regulatory Guide 1.33,

Revision 2.

NRC Regulatory Guide 1.33, Appendix A, requires implementing

procedures

for maintenance

of minimum shift complement.

The failure to have a

licensed operator in the operator-at-the-controls

area who was dedicated to being

attentive to control room indications and alarms and the associated

restrictions in

mobility is a violation of Procedure

OP1.DC12, "Conduct of Routine Operations"

(VIO 50-323/97006-01).

Conclusions

Informal communications

between the Unit 2 CO and the Unit 1 SCO combined

with other ongoing activities distracted the Unit 1 SCO when assuming the Unit 2

operator-at-the-controls

position.

As a result, the SCO left the control room during

the time he was the designated

operator-at-the-controls

for Unit 2. Consequently,

for a time period of approximately 3 minutes, there was no operator-at-the-controls

for Unit 2.

Untimet

0 erator Res

onse to SG Nozzle Dam Alarm

Ins ection Sco

e 71707

On May 15, 1996, while touring containment, the inspector noted that the alarm

and control panel associated

with the nozzle dams installed in SG 1-3 was alarming.

Discussion with the radiation protection (RP) technician stationed nearby indicated

that the panel had been alarming for approximately 30 minutes without a response

from operators.

After notifying the SFM of the alarm, the inspector observed that

operators

had arrived at the panel and were responding to the alarm.

The inspector reviewed the licensee's procedure for monitoring SG nozzle dams,

Procedure

OP A-5:III, Revision 0, the annunciator response

to a SG nozzle dam

trouble alarm, AR PK06-10A, Revision 0, the operator training lesson plan on SG

nozzle dams (lesson R956C4), and the Westinghouse

nuclear safety evaluation

checklist applicable to Busitech SG nozzle dams.

Observations

and Findin s

4-

The nozzle dam control panel for SG 1-3 was located outside the bioshield wall on

the 117-foot elevation in containment.

The panel alarmed both locally and remotely

in the control room; however, operators

in the control room were unable to

determine the cause or condition that resulted in the alarm until they respond to the

local control panel in containment.

Discussion with the cognizant engineer for the nozzle dams indicated that numerous

nozzle dam control panel alarms were occurring foi SG 1-3 due to air leakage past

the mechanical seal

~ This resulted in a buildup of air pressure

between the nozzle

dam wet and dry seals, which caused the alarm.

This pressure

is monitored and

alarmed because

a buildup of pressure

in this volume could be indicative of an air

leak in either the wet or dry seal.

AR A0433176 documented

the occurrence of

multiple nozzle dam alarms during Outage

1R8.

Procedure

OP A-5:IIIrequires that nozzle dam alarms be promptly investigated

and

resolved,

and that a failure of either the wet or dry seal may require that the reactor

vessel level be lowered to mid-loop to make repairs.

No other guidance

is provided

regarding the time frame for operator response.

Discussions with the director of

operations indicated that taking 30 minutes to respond to SG nozzle dam alarm was

not considered

prompt and was not in keeping with management

expectations,

especially if the alarm was a valid indication of a nozzle dam air leak.

A review of training records showed operators

have received training on SG nozzle

dams prior to Outage 1R8.

The training covered the basic construction and

operation of the nozzle dam as well as the operator response

upon receipt of an

alarm.

The training referenced the annunciator response

procedure

and the

operations procedure for the nozzle dams.

The annunciator response

procedure was

noted to be incomplete in that it only listed the conditions that would cause

an

alarm, but it did not provide operators with any guidance

on alarm response

or

reference other procedures.

Other than the problem noted with the annunciator

response

procedure,

the SG nozzle dam training and procedures

appeared

adequate.

The operations director indicated that different alternatives were being considered to

ensure more timely response

to SG nozzle dam alarms during the next outage.

Conclusions

The procedure for response to SG nozzle dam alarms specified that nozzle dam

alarms shall be promptly investigated

and resolved, yet operators took

approximately 30 minutes to respond to an alarming condition.

This was

considered to'be untimely response to the alarming condition by operations

management

and the inspector.

-5-

01 A

Pre arations for the Conduct of Mid-Loo 0 erations

a.

Ins ection Sco

e 71707

The inspector reviewed the licensee's

procedures

and 'preparations for conducting

midloop operations following the completion of core reload and SG inspections.

The

inspector observed tailboards conducted

by the operations services manager and

SFM prior to commencing reduced inventory operations.

b.

Observations

and Findin

s

Preparations

and controls for performing mid-loop operations were observed

by the

inspectors

and determined to adequately

ensure that the appropriate conditions

were established

and maintained during the time the reactor coolant system was in

reduced inventory.

Briefings conducted

prior to the evolution were comprehensive

and thorough.

Questions raised during the briefings were resolved prior to

continuing.

Operators were, provided time to review the procedure

prior to the commencement

of the draindown.

Control room activities were limited during the preparations

in

order to prevent distractions to the operators.

Contingencies

were discussed,

as

well as the actions that would be taken in the event that RHR pump suction was

lost.

These discussions

included the time frames that operators would have to

respond

and the time to boil when at reduced inventory conditions.

The inspector questioned

the fact that not all of the RCPs were re-coupled and off

of their backseat prior to draining to mid-loop.

This appeared to create the potential

for a cold leg vent path that would inhibit the restoration of RHR flow in the event

that pump suction was lost.

The licensee explained that the hot leg vent path, via

the reactor vessel head, would be established

at approximately 20 psig pressure

in

the reactor coolant system.

An analysis that had been performed by Westinghouse

determined that the RCP would not liftoff it's backseat until reactor coolant system

pressure was greater than 20 psig; therefore, the uncoupled and backseated

RCPs

did not create

a credible cold leg vent path.

The inspector determined that this

engineered

pressure

boundary had been determined through engineering

analysis,

undergone

a detailed review by the licensee and appeared

acceptable.

C.

Conclusions

Preparations

by the licensee for the conduct of mid-loop operations were methodical

and thorough.

Operators were given an appropriate amount of time to review and

resolve questions

about the procedure.

Operations management

provided adequate

oversight of the activity and limited unrelated activities in the control room.

-6-

01.5

Seismic Qualification of the 4160V Switch ear

a.

Ins ection Sco

e 71707

The inspectors conducted

routine walkdowns of safety-related

equipment to verify

both availability and proper alignment of components

required for the current

operating mode.

b.

Observations

and Findin s

On April 30, during a walkdown of the Unit 2 4160V switchgear, the inspector

noted that three of the four seismic restraining bolts on the front of breaker

Cubicle 52-HH-15 were only finger-tight (bolt heads were able to be turned freely by

hand).

Breaker Cubicle 52-HH-'l5 houses the breaker for the Sl Pump 2-2 motor.

Due to the potential impact on the seismic qualification of the breaker cubicle, the

inspector immediately notified the unit SFM. An operator was dispatched

and the

bolts were properly tightened.

On May 6, the operations director identified a loose restraining bolt on the upper

door of breaker Cubicle 52-HH-13 in Unit 1.

Breaker Cubicle 52-HH-13 houses the

auxiliary feeder breaker for 4160V Bus H. The identified condition impacted the

seismic qualification of the breaker cubicle and the operability of one of the two

offsite power sources to Bus H. The condition was immediately corrected at the

direction of the of the Unit 2 SFM.

Operations Department Policy B-24, Revision 8, "Vital 4kV Switchgear Operability,"

provides specific guidance to operations

personnel

regarding the seismic

qualification requirements of the 4160V switchgear.

Policy 8-24 states that:

"If any bolt is missing or not properly installed in the upper front door of a

cubicle, the component fed by that breaker must be declared inoperable.

"Iftwo or more bolts are missing or not properly installed in the lower front

door of a cubicle, the component fed by that breaker must be declared

inoperable."

These criteria are based upon the licensee's

seismic analysis for qualification of the

4160V vital busses.

Applying these criteria to the circumstances

noted above

results in the conclusion that Sl Pump 2-2 arid auxiliary power to Unit 1 4kV Bus H

were inoperable until operators tightened the bolts in question.

Subsequently,

the

licensee performed

a detailed analysis of the as-found conditions and determined

that the Sl pump breaker was operable.

A review of the maintenance

history associated

with Sl Pump 2-2 noted that the

pump. was in a maintenance

outage window during the second week of April.

Following the maintenance,

the breaker was racked in'and the cubicle doors secured

-7-

on April 10.

The rack-in of Breaker 52-HH-15 was documented

on Attachment 9.1

of Procedure

OPJ-6A:IV, Revision 15, "4160 Volt Breaker Code Order."

Step 5.3

of Procedure

OP J-6A:IV requires all breaker cubicle panels and doors to be fully

bolted closed to ensure structural integrity of the bus housing for postulated

seismic

events.

To meet this requirement, Attachment 9.1 provides

a specific step to

tighten the bolts on the cubicle doors until the split ring washer is flat and then an

additional 1/8 to 1/4 turn.

This step was initialed as completed by the operators

who racked in Breaker 52-HH-15 on April 10.

The licensee has not identified any

additional records to indicate that the cubicle doors for Breaker 52-HH-15 had been

opened after April 10.

A review of the activities associated

with the auxiliary feeder breaker to Unit 1 4kV

Bus H, found that the auxiliary transformer feeding the breaker was re-energized

during the nightshift on May 5 (restoring the operability of auxiliary power to the

unit}. Since the operations director identified the loose bolt on the breaker cubicle

early in the dayshift on May 6, auxiliary power to Bus H was inoperable for

approximately an additional 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> following the re-energization of the

transformer.

Unit 1 was defueled during this event and the operability of auxiliary

power to Bus H was not required by plant TS.

Unit

1 4kV Busses

F and G were

operable during that period.

The licensee's self assessment

from 2R7 noted that multiple breaker cubictes on a

vital bus were found with missing or loose bolts which rendered the bus inoperable

when it was required by the outage safety plan.

This additional failure to properly secure fasteners

as required to ensure the

operability of the power source for SI Pump 2-2 in accordance

with approved

procedures,

therefore,

is a violation of 10 CFR Part 50, Appendix B, Criterion V,

which requires, in part, that activities affecting quality shall be accomplished

in

accordance

with these instructions, procedures,

or drawings (VIO 50-323/97006-

02).

The licensee has initiated actions to perform periodic checks of vital bus fasteners

to ensure that they have been properly tightened in order to detect and correct the

improper installation of fasteners.

Conclusions

A violation was identified in that controls established to ensure vital breaker cubicle

seismic restraints were ineffective in ensuring the proper installation of the

fasteners.

Subsequent

analysis showed the breaker to be operable with the loose

fasteners.

Similar problems occurred during Outage 2R7 and corrective actions had

not been fully effective in preventing additional instances.

-8-

01.6

Return to Service of the Main and Auxiliar Transformers

a.

Ins ection Sco

e 71707

The inspectors observed the operators return the main and auxiliary transformers to

service in accordance with Procedure

OPJ-2:I, Revision 7, "Main and Aux

Transformer Return to Service."

b.

Observations

and Findin

s

The energizing of the main transformer was performed as part of an electrical

system realignment to support replacement of Startup Transformer

1-1 during the

Outage 1R8.

The coordination of several procedures

including a temporary

procedure to energize the 12kV startup bus from the auxiliary power was necessary

to support the startup transformer replacement.

The personnel performing the

procedure

used good three way communications,

self-checking and peer checking

as applicable.

The activities included verifying the status of ground buggies, racking

in 12kV and 4kV breakers,

and fuse installation.

The personnel were observed

using appropriate safety equipment, including "flash suits" and a high voltage "hot

stick."

C.

Conclusions

Energizing the main and auxiliary transformers was performed well, with good

coordination of several procedures.

The personnel

involved were knowledgeable

of

the plant equipment and the procedure requirements

and performed the activities in

accordance

with the applicable procedure

and appropriate safety precautions.

01.7

Fill and Vent of the RHR S stem

Char in

Pum

s and Char

in

Flow Path

a.

Ins ection Sco

e 71707

The inspectors observed the operators filland vent the RHR system and portions of

the chemical and volume control system (CVCS) in accordance

with

Procedure OPA-2:Vll, Revision 6, "Core Offload Window Systems Restoration."

b.

Observations

and Findin s

A SFM was coordinating the activities of several teams in different areas of the

plant to perform this evolution.

The evolution included fillingthe piping systems

from the refueling water storage tank.

When the charging injection lines were filled,

the operators noted an increasing level in the reactor coolant drain tank.

The

operators closed valve CVCS-1-8108, isolating the flow path through the

regenerative

heat exchanger

and successfully terminating the flow to the reactor

'oolant drain tank; This expedited the identification and isolation of the leak path:

Further investigation revealed that the drain valves from the charging line

-9-

downstream of the regenerative

heat exchanger

(CVCS-1-91 and CVCS-1-566)

were

open.

These valves had been documented

as closed 2 days earlier.

Throughout this evolution, this portion of the CVCS was not required to be operable

or in operation.

The licensee wrote an AR to document this problem.

Subsequent

evaluation by the

licensee was inconclusive as to the cause of the out-of-position valves; however,

the licensee concluded that the most'ikely cause was operator error during valve

repositioning.

During the evolution, the operators were observed to be very knowledgeable of the

equipment, the procedure,

and activities being performed.

They were aware of

plant conditions and properly factored those conditions into their performance of the

procedure.

Communications

were clear with the use of three way dialogue.

The

SFM and CO were informed of the evolution progress, with frequent updates.

These

activities were generally well coordinated, with the exception of unblocking of

spring cans, which delayed the start of the RHR pump.

This problem involved

operators

needing to request unblocking supports twice from the maintenance

organization.

c.

Conclusions

The evolution had been well planned and was accomplished

in a cautious and

deliberate manner.

The operators demonstrated

excellent knowledge of the

equipment operation and interactions,

The actions taken to identify and isolate the

leak were sound and effective.

The regulatory and safety significance of the valve

mis-alignment was minimal since the system was not required to be operable.

Coordination between operations

and maintenance

were less effective and resulted

in delays but did not significantly impact the evolution.

01.8

Observation of 0 erations Activities Durin

Refuelin

Outa

e 1RS

a.

Ins ection Sco

e 71715

The inspector observed control room activities toward the end of Refueling

Outage

1R8, in order to evaluate operator performance

under the higher stress and

activity conditions associated

with preparations for unit return to power operation.

Observations

were conducted from May 20 through May 22, 1997, and focused

into the following areas:

~

Observation of equipment clearance activities, with emphasis

on how

effectively each individual involved in the process fulfilled their

responsibilities

as defined in the newly revised clearance

procedure.

Field walkdown of several clearances to confirm compliance with procedure

requirement's.

-10-

Observation of operator performance of control room activities associated

with outage completion, and operations interaction with other plant

organizations

disciplines involved in outage completion.

b.

Observation

and Findin s

Operations command and control was good during a period of a high work

activity and problem challenges.

In particular, the operating crew worked

well together and properly evaluated

and responded

to a loss of cold

calibrated pressurizer level indication, and an unexpectedly

high volume of

reactor coolant degassing,

which impacted reactor vessel head venting

operations

and repair work on an RCP.

The SFM effectively identified, documented,

and resolved minor problems

.

associated

with an improperly signed clearance,

and an improperly validated

test procedure.

Control room personnel communicated

well throughout the observation

period.

Specifically, operator peer checking and repeat-back

identified and

corrected several problems during operational transitions.

Examples included

identification that an operator was at the wrong switch for a valve position

change

and an'perator was about to make an incorrect public address

announcement

for start of an RCP.

Field walkdown of numerous clearance points identified no discrepancies.

Considering the magnitude of change implemented to the clearance

process

prior to the outage, operator training on the new changes

did not appear to

be timely or comprehensive.

Most operators stated that they were not

comfortable with such significant changes

immediately prior to an outage,

and they did not consider that training appropriately emphasized

the specific

new responsibilities affecting each individual involved in the clearance

process.

For example, some operators stated that they were not aware of

additional requirements for redundant verification of individual clearance

points until pointed out by the individuals they were relieving at shift change.

As a group, operators did not appear to have fully "bought-in" to the revised

clearance

process.

Although operators clearly recognized the need for

additional controls to prevent recurrence of previous clearance problems,

some appeared to view the process

as overly-cumbersome,

and did not fully

accept the need for the magnitude of redundant over-checking involved in

the new procedure.

Some operators

also noted a sense of management

reluctance to appropriately consider operator opinion in developing the new

process.

Recognizing the major effort and careful consideration

involved in

the licensee's

revision of its clearance

process, the inspector considered that

0

-1 1-

more interactive training on the bases for the changes

would have benefitted

all involved.

c.

Conclusions

The operations shift supervisor and SFM demonstrated

good command and control

during preparations for return to power operation at the end of Refueling

Outage

1R8.

Operator peer checking was consistently implemented and was

effective in identifying and correcting minor problems before they occurred.

Operator training on major changes to the equipment clearance

process prior to the

outage did not appear to have fully covered all appropriate aspects of new

responsibilities for each individual involved in the new process.

Also, additional

training on the bases for significant clearance process changes

appeared

warranted

to ensure full operator understanding

and support of the need for implemented

changes,

08

Miscellaneous Operations Issues (92901)

08.1

Closed

Licensee Event Re ort

LER 50-323 96004:

fuel movement not

suspended

when source range audible indication stopped.

On May 4, 1996, an

engineer entered containment

and noted that the source range audible indication

was not present with core alterations in progress.

The refueling senior reactor

operator was notified, who in turn notified the control room. A control room

operator immediately re-established

the audible indication.

The licensee

subsequently

determined that audible indication had been lost for approximately

1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />.

The licensee identified that the sealer timer, which had been powered from a

convenience

outlet, momentary lost power during a switching operation and

required resetting to reestablish count rate indication.

The licensee determined that

had the sealer timer been powered from the audio count rate drawer, the switching

operation would not have affected the component.

The licensee revised

Surveillance Test Procedure

(STP) I-4C, "Calibration of Audio Count Rate/Sealer

Timer Channel," to include a step to specify the exact location to plug in the sealer

timer.

In addition, the licensee initiated actions to provide an alarm to alert

operators of a loss of audible counts.

The inspectors noted that the alarm was

installed and used during the recent Unit 1 refueling outage and

Procedure

STP 1-4C was revised.

TS 3.9.2 requires, in part, that continuous

audible indication count be available in

the control room and containment,

or suspend

all operations involving core

alterations.

The inspectors determined that the licensee did not violate the

requirements

of TS 3.9.2 since audible count indication was immediately

reestablished

when discovered although audible indication had been lost for

approximately

1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />.

-1 2-

The inspectors determined that Procedure

STP l-4C, Revision 3, did not contain

adequate

guidance

on installing the power supply to the sealer timer, and therefore,

was not appropriate to the circumstances,

constituting

a violation of 10 CFR Part 50, Appendix B, Criterion V, "Procedures."

This licensee-identified

and

corrected violation is being treated as a non-cited violation, consistent with

Section VII.B.1 of the NRC Enforcement Policy (NCV 50-323/97006-03).

The inspectors documented

a previous event on November 6, 1995, where the

operators failed to recognize that the audible count was not on when Unit 1 was in

Mode 6 (NRC Inspection Report 50-275;323/95016).

The inspectors concluded

that these two examples indicated

a lack of operator awareness

and sensitivity to

the requirement to maintain audible count indication in the control room and

containment.

II. Maintenance

M1

Conduct of Maintenance

M1.1

Maintenance

Observations

a.

Ins ection Sco

e 62707

The inspectors observed

all or portions of the following work activities:

~

C0152057, Replacement

of Pressurizer

Level Transmitter (LT-461)

~

C01488866, Installation of Component

Cooling Water Valve TCV-130

~

C0146604, Installation of Battery 1-3

b.

Observations

and Findin s

The inspectors found the work performed under these activities to be accomplished

in accordance

with procedures.

All work observed was performed with the work

package present and in active use.

QC personnel were at the work location as

required.

C.

Conclusions

For the maintenance

activities observed

both technical maintenance

and mechanical

maintenance

personnel were knowledgeable

of the assigned tasks; they had

appropriate authorization for the work and closely followed the work package

instructions.

-1 3-

M1.1.1

Installation of Ground Bu

a.

Ins ection Sco

e 62707

The inspectors observed

portions of Maintenance

Procedure

(MP) E-57.11B,

"Protective Grounding," Revision 15.

b.

Observations

and Findin s

Technical Maintenance

and Operations personnel installed a ground buggy in

electrical Cubicle 52-HG-5 (for 4160V. Diesel Generator

1-2) in accordance

with

Procedure

MP E-57.11B.

The personnel

used the required personnel safety

equipment; the test equipment was properly used to verify the bus, and line sides of

the breaker were de-energized.

The first ground buggy used was found to stick in

the elevating mechanism

due to interference between the rails. The personnel

identified the cause of the problem and stopped the activity in order to prevent

damage to the equipment.

The ground buggy was replaced and the installation was

completed.

C.

Conclusions

The installation of the ground buggy was performed in a safe and cautious manner.

M'l.1.2 Clean

Ins ect

and Test 480V Circuit Breakers

a.

Ins ection Sco

e 62707

The inspectors observed portions of the following surveillance and maintenance

procedures:

~

MP E-64.1A

AC and DC Molded Circuit Breaker Test Procedure,

Revision 28

STP IVI-83A

Penetration Overcurrent Protection, Revision 16

b.

Observations

and Findin s

Technical Maintenance

personnel cleaned, inspected,

and tested circuit breakers on

the Bus 1F 480 volt bus.

Two breakers failed the surveillance acceptance

criteria

established to protect containment electrical penetrations

from overcurrent.

Containment

Fan 1-2 backup overcurrent Breaker 52-1F-01R failed to trip in the

required time and the FCV-750 circuit Breaker 52-1F-23 failed to trip at less than

the penetration's

maximum current limit. In each case,

an additional 10 percent of

the same class breakers were tested,

as required by TS, and no additional failures

occurred.

Other breakers tested passed

the surveillance acceptance

criteria, but

failed the more stringent manufacturer's

tolerance and were replaced.

The test

-14-

equipment was observed to be within current calibration.

Proper safety precautions

were used, and procedures

were followed and signed as required.

The cognizant

system engineer'was

closely involved with the work and the resolution of problems

as they arose.

c

~

Conclusions

The inspectors found the work performed under these activities to be accomplished

in accordance

with procedures.

All work observed was performed with the work

package present

and in active use.

System engineers

closely monitored job

progress.

M1.1.3 Containment

Fan Cooler Unit CFCU

1-4 Motor Ali nment and Electrical

Terminations

a 0

Ins ection Sco

e 62707

The inspectors observed portions of the following work order C00152198 to

replace bearings

and inspect the motor for CFCU 1-4.

b.

Observations

and Findin

s

Mechanical Maintenance

personnel performed motor alignment per

Procedure

MP M-56.19 and Technical Maintenance

personnel

performed the

electrical termination per MP E-57.2B.

The test equipment was observed to be

within calibration.

The procedure was at the job site and the steps were signed as

they were performed.

The two activities were well coordinated

between the two

maintenance

organizations to minimize the time for transition between groups.

During the termination activity, the licensee identified that the Raychem material

installed on the motor lead butt splices was outside the required size for the

application.

These splices were believed to have been installed in 1985.

The

licensee inspected the other Unit 1 CFCUs and found similar discrepancies.

The

splices were all replaced prior to the restart of the unit.

Unit 2 was evaluated for

operability and found acceptable with plans for inspection and repair during a later

outage.

C.

Conclusions

The composite maintenance

crew worked well together.

Work activities were

performed in accordance

with the procedural requirements,

and were well

coordinated to minimize the time necessary to complete this critical path

maintenance.

The licensee's identification and response to the undersize

Raychem

splicing appeared to'orrect the deficiencies.

0

-1 5-

M1.1.4

Removal

Ins ection

and Installation of RCP Mechanical Seal

a.

Ins ection Sco

e 62707

The inspectors observed

performance of portions of Procedure

MP M-7.43,

"Removal, Inspection, and Installation of Mechanical Seat-RCP (Motor In Place),"

Revision 14.

b.

Observations

and Findin

s

Following planned outage maintenance

on the RCP 1-4 seal assembly, the number

one seal leaked when filling the reactor coolant system.

Mechanical Maintenance

personnel

removed and inspected the mechanical seal, in accordance

with

Procedure

MP M-7A3. To minimize the radiation exposure to personnel, the

individual in the motor support stand wore a camera with the image displayed in a

nearby low-dose area and recorded

on videotape.

The inspection revealed several

paint chips on the seal in the area of the suspected

leak, including one paint chip

that appeared

to interfere with the o-ring seal.

The seals were cleaned,

a new

o-ring installed, and the seals reassembled.

f

Involved maintenance

personnel were knowledgeable

of the procedure,

tools, and

equipment and demonstrated

good teamwork.

They used good radiological

practices to minimize the spread of contaminatior., stopping to wipe up water and

clean the exposed

surfaces

as they worked.

Weakness

in foreign material exclusion was evident from the paint chips found in

the seal area.

Although the workers continually cleaned

as they worked, the

methods used did not prevent the introduction of foreign material. At the time of

the seal disassembly,

the inspectors noted that persorrnel were carrying hoses and

outage material across the open grating above the RCP.

Additionally, chain-falls

used in the disassembly

and reassembly of the seals had apparently chipped the

paint on the inside of the motor support stand, which may have been the source of

the foreign material that caused the unacceptable

seal leakage.

C.

Conclusions

The activities related to the removal, inspection, and repair of the RCP 1-4 seals

were observed to have been performed in accordance

with the procedure.

The use

of the camera and monitor was effective in reducing radiation exposure for the task.

However, the previous efforts to prevent foreign material from entering the seals

were ineffective, which resulted in the need for the rework of the RCP seal.

-1 6-

M1.2

Surveillance Observations

Ins ection Sco

e 61726

Selected surveillance tests required to be performed by the TS were reviewed on a

sampling basis to verify that:

(1) the surveillance tests were correctly included on

the facility schedule;

(2) a technically adequate

procedure existed for the

performance of the surveillance tests; (3) the surveillance tests had been performed

at a frequency specified in the TS; and (4) test results satisfied acceptance

criteria

or were properly dispositioned.

The inspectors observed

all or portions of the following surveillances:

~

STP M-16T

Slave Relay Test of K615A/8, K612A, and K614B (Sl

and Phase A Isolation), Revision 3

~

STP P-23A

Acceleration Timing of Safety-Related

Pumps Actuated

By Solid State Protection System Train A, Revision 5

~

STP P-23B

Acceleration Timing of Safety-Related

Pumps Actuated

By Solid State Protection System Train B, Revision 6

~

STP P-23C

Acceleration Timing of Turbine Driven Auxiliary

Feedwater Pump, Revision 12

~

STP V-5C

Emergency

Core Cooling System Hot Leg Check Valve

Leak Test, Revision

11

~

STP R-1B

~

STP R-31

Rod Drop Measurement,

Revision 17

Rod Worth Measurements

Using Rod Swap Method,

Revision 7

b..

Observations

and Findin s

The inspectors found that the surveillances

observed were being scheduled

and

performed at the required frequency.

The procedures

governing the surveillance

tests were technically adequate

and personnel performing the surveillance

demonstrated

an adequate

level of knowledge. The engineering test directors were

well versed on the technical requirements

of the testing and closely monitored test

performance

and scrutinized test results.

The inspectors noted that test results

appeared to have been apprcpriately dispositioned.

0

-1 7-

M1.2.1

Manual and AUTO Transfer of 4KV Vital Busses Off-site Power Sources

a.

Ins ection Sco

e 61726

The inspector observed the performance of Procedure

STP M-13A, "Manual and

Auto Transfer of 4kV Vital Busses Off-site Power Sources,"

Revision 6, to

determine whether the procedure was technically adequate

and the test results

satisfied acceptance

criteria or were properly dispositioned.

b.

Observations

and Findin s

While performing the manual transfer of 4KV vital Bus H from the auxiliary

transformer to the startup transformer,

in accordance

with Procedure

STP M-13A,

Revision 6, the operators noted that the incoming bus voltage was 10 volts higher

than the running bus voltage.

A design change

had been installed during

Outage IRS which provided

a variable tap transformer and added the ability to

change the startup bus voltage from the control room.

Operations normal operating

procedure for this transfer, Procedure

OP J-6 A:II, had been updated with

instructions to match voltages within indicated 3 volts; however, the surveillance

procedure

had not been updated.

As a result, operators stopped the surveillance

test in order to resolve the difference in voltage by revising the procedure to include

the necessary

instructions.

The test was then completed satisfactorily.

Conclusions

Operators proceeded with caution after revising Procedure

STP M-13A to provide

instructions for utilizing the newly installed variable tap transformer for adjusting

startup bus voltage.

Surveillance procedure reviews performed prior to

implementation of the design change failed to identify the need for the change.

M1.2.2 Containment

Ins ection Prior to Establishin

Containment Inte rit

a.

Ins ection Sco

e 61726

The inspectors observed portions of Procedure

STP M-45A, "Containment

Inspection Prior to Establishing Containment Integrity," Revision 6.

b.

Observations

and Findin s

The conditions in the containment were noted to be in compliance with the criteria

of Procedure

STP M-45A. All noted exceptions to the closeout were documented

and tracked by the licensee.

A minimal amount of debris including tape, a sheet

metal screw, paper clips, a test fitting cap, and plastic mounting tabs were

identified to the licensee

and corrected.

The general area containment cleanup 'was

complete, with the exception of several last maintenance

activities.

Some

-1 8-

insulation fasteners

on the SGs and reactor coolant system piping were noted to be

loose or broken.

The licensee corrected these discrepancies.

c.

Conclusions

Containment closeout activities were appropriately controlled.

Several minor

discrepancies

were noted by inspectors

and corrected by the licensee.

M1.2.3 Resettin

Hi h Flux Bistables

Unit

1

a.

Ins ection Sco

e 61726

On June 6, 1997, the inspectors observed Technical Maintenance technicians

perform portions of Procedure

STP l-2U, "Resetting High Flux Bistables for Power

Range Channels,"

Revision 9A.

b.

Observations

and Findin s

The technicians

used good communication techniques

between themselves

and

with the operators.

In addition, the technicians proceeded

cautiously when opening

the power range drawers to avoid component damage

and used good procedure

adherence throughout'he surveillance test.

c.

Conclusions

The inspector concluded that the technicians displayed an overall strong

performance during the surveillance test.

M6

Maintenance Organization and Administration

M6.1

Outa

e 1RS Safet

Plan and Schedule

a.

Ins ection Sco

e 62707

The inspector reviewed the licensee's

Outage Safety plan and schedule

and

attended

Outage Coordination Center meetings during the course of the outage.

b.

Observations

and Findin s

Significant effort was put forth by the licensee in the development of the outage

safety plan and schedule.

Efforts in this area appeared to be focused on

maintaining multiple sources of power and core cooling capabilities during the

different phases of the outage.

Particular emphasis was placed on communicating

these requirements to all personnel

in the organization on a daily basis.

Changes

in-

the schedule

and scope of work were carefully evaluated as to the potential impact

-19-

on the outage safety plan.

Changes

were made when required and approved

by the

Plant Staff Review Committee (PSRC).

The outage safety plan also placed emphasis

on maintaining the availability of the

containment sump at different stages of the outage.

The inspector noted during

tours of containment tnat there were materials and plastic on the 91-foot elevation

of containment that had the potential to partially block the sump.

After questioning

the licensee on the control of material, the licensee acknowledged that a review of

the control and storage of material on the 91-foot level of containment was

warranted.

One discrepancy was noted and corrected by the licensee where work was

conducted

contrary to the outage safety plan.

Turbine building siding work was

allowed to continue above the Unit 2 startup transformers during the time that

startup power was being relied upon as the single source of offsite power.

The

siding work posed

a threat to the Unit 1 offsite power.

Review of the situation

revealed that, while the siding work had been approved

early in the outage, the

licensee had not established

adequate

subsequent

controls to assure that personnel

understood the actions required when plant conditions changed.

As a result, the

licensee failed to ensure that the work being performed did not threaten the single

source of offsite power.

C.

Conclusions

The outage safety plan and schedule were focused on maintaining a safe plant

configuration in order to ensure availability of emergency power sources

and core

cooling throughout the outage when there was fuel in the reactor vessel.

The

safety plan and schedule were clearly communicated to the organization in meetings

and daily reports that were published and distributed to workers.

M7

Quality Assurance

in Maintenance Activities

M7.1

Licensee Qualit

Assessments

of 1RS Performance

a.

Ins ection Sco

e 40500

The inspector reviewed the licensee's

self assessments

of the first two outage

windows during Outage

1R8 as well as the overview assessment

of the previous

Refueling Outage 2R7.

b.

Observations

and Findin

s

The licensee assessments

covered operations,

maintenance

and engineering

services,

and areas common to all, which were considered

as cross functional

areas..'The

assessments

were issued within several days. after the completion of,

-20-

the assessment

periods.

This provided plant management

with timely feedback on

performance

and focused management's

attention on the problem areas, which

were of greatest significance.

The assessments

noted improvement in two of the three areas that were of concern

during the last outage.

Specifically, performance

in the areas of personnel safety

and foreign material exclusion had improved, while a significant number of

performance errors continued to occur with clearances.

Clearance

Errors Durin

Outa

e 1R8

Clearance discrepancies

were predominantly personnel performance

errors and did

not appear to be due to procedural inadequacies.

The inspector reviewed the types

of errors that were documented

and concluded that the causes for the errors were

mostly in the areas of inattention to detail, knowledge level exceeded,

and time

pressures.

The inspector noted that several significant clearance

errors occurred, including:

a

valve and a 480 volt breaker which had been tagged

in the incorrect position; work

performed without clearances

when a clearance was required; and reporting off

clearances

prior to the completion of work. These errors did not result in personal

injury or damage to equipment, but were viewed by the inspector as precursors to

potentially more significant events and, therefore, warranted additional attention

from licensee management.

Since problems with clearances

had been a problem

area during the last outage the licensee's

self assessment

concluded that corrective

actions to address

problems with clearances

were not comprehensive

and, thus,

partially ineffective.

The NQS assessment

noted that the actions taken by

management

during the first two outage windows had a p'ositive effect on clearance

performance for the remainder of the outage.

C.

Conclusions

NQS assessments

of performance during 1R8 were effective in identifying problem

areas to plant management.

Assessments

were issued in a timely manner and

provided management with the information needed to focus attention on problem

areas.

A significant number of clearance performance problems occurred during

Outage 1R8. The licensee's efforts to improve performance

in this area immediately

after Outage 2R7 appeared to have been not completely effective in preventing

similar problems.

M8

Miscellaneous Maintenance issues (92902)

M8.1

Closed

LER 50-275 83040:

missed inservice inspection (ISI) surveillance.

On

.

April 10, 1996, the licensee'identified that since the initial fuel loading in both units,

-21-

the RHR and excess letdown heat exchanger

seismic supports were not included in

the ISI'program plan or routinely inspected

as required by TS 4.0.5.

On April 11,

1996, the licensee inspected the seismic supports

and found them acceptable.

The licensee performed

a review of maintenance

records and noted no indication of

inoperability or required maintenance

during the period of the missed surveillance.

Therefore, the licensee concluded that while the seismic supports were technically

inoperable, they were available during that period of time to support the heat

exchangers

as required during a seismic event.

ISI and engineering

personnel

performed

a walkdown of components to ensure the

attached

seismic supports were properly identified and inspected.

The licensee

identified no additional missed surveillances.

The licensee revised the ISI program

plan and ISI surveillance schedule to include the RHR and excess letdown heat

exchanger

seismic supports.

The inspectors reviewed the ISI program plan and

observed that it included the heat exchanger supports.

The inspectors concluded

that the licensee's corrective actions were appropriate.

TS 4.0.5 requires,

in part, that tests and inspections

be performed in accordance

with periodic surveillance criteria of Section XI of the ASME Code.

The Section XI

for the RHR heat exchanger

and excess letdown heat exchanger

requires, in part, an

inspection in accordance

with the visual test criteria be performed prior to placing

the system in use and each 40 month period thereafter.

The failure to perform the

surveillance

is a violation of TS. This licensee-identified

and corrected violation is

being treated as a noncited violation, consistent with Section VII.B.1 of the NRC

Enforcement Policy (NCV 50-275;323/97006-04).

III. En ineerin

E1

Conduct of Engineering

E1.1

RCP Oil Collection S stem Discre ancies

a.

Ins ection Sco

e 37551

92903

The inspector reviewed the licensee's

actions to identify and resolve reactor coolant

lube oil collection system problems.

The NRC highlighted potential problems in

IN 94-58, "RCP Lube Oil Fire." During the course of the inspection, the following

documents were reviewed:

AR A0351025, Evaluation of IN 94-58

Operational Events Assessment

Log 94-330

~ '

AR A0429325,

1RB RCP Oil Collection System Inspection Results

-22-

Independent

Safety Engineering

Group (ISEG) Assessment

Report 961430034, Assessment

of RCP Oil Collection System to the

Requirements

of 10 CFR Part 50, Appendix R

Operability Evaluation 97-04, Revision 0, Operability of the RCP LiftOil

System with Missing Oil L'ift Pump Enclosures

(Unit 2)

b.

Observations

and Findin s

Ins ection of RCP Oil Collection S stem durin

1R8

On April 19, 1997, the licensee documented

the inspection results for Unit 1 RCP

oil collection piping on AR A0429325.

The AR noted that several of the RCP oil

collection systems

had missing or bent and broken tray sections

as well as tray

sections that were in need of adjustment.

During the inspection licensee personnel

noted that there was a small section of the

liftoil pump instrument tubing that was pressurized

during liftoil pump operation

that was not enclosed

by a sheet metal shield.

This was noted as not being in

accordance

with licensee procedures

which implement the requirements of the fire

protection program to confine a leak within the shield and to direct the oil.to

collection pans.

Following identification of this discrepancy,

the licensee made a 'l-

hour non-emergency

report to the NRC to report a condition

outside of the design

basis of the plant.

The licensee noted that the section of tubing was not normally

pressurized

during RCP operation and that the only time the line was pressurized

was during an RCP start.

Reviews determined that the RCP lift oil system had been modified to add the

additional section of tubing that was outside of the spray shield.

The licensee

determined that the modifications were most likely made sometime in 1977 or

1978; however, no records or documentation of the modification were found.

Licensee Determination of Acce tabilit for Continued 0 eration

The licensee issued

a prompt operability assessment

(POA) for Unit 2 since it was

not practical to correct the liftoil shield discrepancies

until the next outage due to

the radiation levels in the RCP cubicles where the unshielded instrument tubing is

located.

Unit 1 was not included in the evaluation since 1R8 was ongoing at the

time of discovery and the licensee planned to correct the discrepancies

prior to the

restart of Unit 1.

The POA was later replaced by an operability evaluation that was reviewed and

approved

by the PSRC.

The licensee's conclusion on operability was based on the

line being pressurized

only during pump starts and the ability to monitor for oil

~ losses.

'The licensee initiated compensatory

actions for observation of-piping leaks

during RCP starts.'he

inspector reviewed the assessment

and determined that it

.~

-23-

appeared

to be reasonable

and included adequate

compensatory

measures.

The

licensee intends to correct the Unit 2 deficiencies during the next Mode 3 entry, not

to exceed Outage 2R8.

Licensee Evaluation of IN 94-58

NRC IN 94-58, "RCP Lube Oil Fire," addressed

a number of discrepancies

associated

with the RCP oil collection systems

in which inadequately

designed,

installed, and maintained oil collection systems resulted in fire hazards.

The

inspectors performed

a walkdown of the system during Refueling Outage

1R8 and

at the end of the outage prior to restart.

The licensee received IN 94-58 in August 1994.

In September

1994, the licensee's

OEA log indicated that Diablo Canyon's

RCP oil collection system did not utilize

PVC piping as described

in IN 94-58.

Evaluation of other aspects of IN 94-58

involving oil on insulation and RCP oil collections system design adequacy,

installation, and maintenance

were not addressed

at that time.

AR A0351025 was later written by the licensee to track the evaluation of IN 94-58.

No inspections were performed by licensee personnel

until June 1996 for Unit 2 and

April 1997 for Unit 1, despite the fact that there had been several refueling outages

and forced shutdowns which had offered inspection opportunities.

As of April

1997, however,

IN 94-58 was still being evaluated

by the licensee.

Based upon the licensee's untimely evaluation of IN 94-58, the inspector questioned

their response to other NRC generic communications to the industry.

The licensee

provided a status of evaluations

and the inspector noted that there were nine other

issues in the time period from 1992 through 1994 that had not been fully

evaluated.

The licensee's

response

to these issues will oe reviewed to determine

adequacy

and timeliness.

This is being tracked as an inspection followup item

(IFI 50-275;323/97006-05).

ISEG Assessment

of RCP Oil Collection S stem to the Re uirements of 10 CFR Part 50 A

endix R

In June 1996, NQS performed an assessment

of the Unit 2 RCP oil collection

system.

During the assessment,

it was noted that the actual flash point of the

motor oil was 55 degrees lower than what was stated in the UFSAR and

Supplemental

Safety Evaluation Report 23. This discrepancy was identified as

requiring a 10 CFR 50.59 safety evaluation.

Following the inspectors'uestions,

the safety evaluation was completed and approved

by the PSRC in May.1997,

approximately

11 months after the discrepancy

and the need for an evaluation was

identified.

The safety evaluation concluded that the difference in flash point

temperature

did not create an unreviewed safety question.

-24-

As a part of the ISEG assessment,

a review of 10 CFR Part 50, Appendix R,

requirements

was performed and no discrepancies

were noted.

The assessment

included an observation that the RCP oil collection system was required to be

capable of collecting lube oil from all potential pressurized

and unpressurized

leakage sites.

The Unit 2 RCP oil collection system was inspected with this in mind

and compared the as-constructed

system to the as-designed

system.

No

discrepancies

were noted with regard to this capability during the assessment.

NRC Evaluation of Licensee

Res

onse

TS 6.8.1 requires that procedures

covering the fire protection program be

implemented.

The licensee is committed to implement a lube oil collection system

to contain system leaks through program directive Procedure

OM8, Revision 2, "Fire

Protection Program," and through references to provisions in the FSAR.

The licensee's

response

to IN 94-58 was reviewed and the following observations

were made:

IN 94-58 was issued in August 1994; however, as of April 1997 the licensee

had not perfo'rmed an inspection of the system

as recommended

in the initial

evaluation of the IN. Additionally, the IN remained in an "eval" status

meaning that it had not been determined if corrective action was necessary.

The licensee's

self-assessment

of the Unit 2 RCP oil collection system in

June 1996 incorrectly concluded that the system met the requirements of

10 CFR Part 50, Appendix R, and failed to identify modifications that were

made to the RCP lift oil pump instrument tubing.

Discrepancies

between the flash point temperature

in the UFSAR and the

actual flash point temperature were required to be evaluated to determine the

affect of the difference; however, an evaluation was not completed until the

NRC raised questions about the difference, approximately 10 months after

the initial identification of the discrepancy.

Inspections of the RCP oil collection system performed by the licensee at the

beginning of Outage 1R8 revealed numerous installation and maintenance

discrepancies

that were indicative of inadequate

attention to the system.

NRC Observations

of Plant Confi uration

The inspectors questioned

the use of sealant to fillin gaps between the base of the

RCPs and the collection pans.

The licensee responded that the sealant that had

been used was RTV 732 sealant and had not been qualified for use in containment

and would be replaced with a qualified caulking.

The licensee also reviewed the

calculation for debris clogging the containment sump and determined that the

-25-

additional caulking material, if transported to the containment sump during an

accident, would not significantly reduce the margin to safety in the calculation for

adequate

emergency

core cooling system suction from the sump.

Conclusions

The inspectors determined that the RCP oil collection system spray shield deficiency

was a violation of licensee procedures.

There were opportunities to have identified

the spray shield deficiency and other maintenance

related deficiencies earlier.

This

constituted

a violation of TS 6.8.1 (VIO 50-275/97006-06).

The licensee was slow

to complete

a safety evaluation for a lowered lube oil flash point.

E8

IVliscellaneous Engineering Issues (92903)

E8.1

MFP Turbine Sto

Valve Time Res

onse Testin

Discre ancies

a.

Ins ection Sco

e 92903

A

The inspector reviewed the actions initiated by the licensee following discovery that

MFP turbine stop valves had not been periodically response

time tested.

During the

inspection the following documents

were reviewed.

b.

~

AR AO316782, Revise ISC Procedure

PEP-04

~

AR A0429696, MFP Turbine Stop Valve Testing

~

Quality Evaluation 0011951, MFP Turbine Stop Valve Testing

~

AR A0427518, AE 11, POA addressing

lack of time response

testing

~

TS 3.3.2 Interpretation 97-04, Revision 0

Observations

and Findin s

Identification of the Need to Test MFP Turbine Sto

Valves

The design of the main feedwater (MFW) system relies upon the rapid closure of the

MFW control and bypass valves to limitthe mass and energy release within

containment in various secondary

system rupture accidents.

The design class

II

MFP trip, which occurs concurrently with a MFW control and bypass valve closure

signal, provides the backup in the event that a MFW control valve or it's associated

bypass valve fails to close.

Following a Unit 2 reactor trip in March 1997, NQS initiated a review of past

problems associated

with MFP turbine stop valves.

During the review it was

recognized that no corrective actions had been taken following the previous

discovery of the need to response

time test MFP turbine stop valves.

AR A0316782, written in September

1993, identified that MFP turbine stop valves

and associated

control circuitry were not being periodically time response

tested.

The licensee recognized. that since the MFP trip feature was credited in the main

0

-26-

steam line break mass and energy release analysis, the testing was required and a

surveillance procedure was needed.

There is no TS requirement for response

time

testing of these valves.

Response

time testing of the MFW turbine stop valves had not been previously

accomplished.

The cognizant system engineer later closed out the AR in October

1995, in error, without a surveillance test procedure having been written to test the

valves, and as a result the required testing was not accomplished.

10 CFR Part 50, Appendix B, Criterion XI, "Test Control," requires that a test

program be established

by the licensee to assure that all testing required to

demonstrate

that structures, systems,

and components

will perform satisfactorily in

service is identified and performed in accordance

with written test procedures,

which incorporate the requirements

and acceptance

limits contained

in applicable

design documents.

These requirements

were not met by the licensee until testing

was performed to verify that the time response

of the MFP turbine stop valves and

associated

circuitry were verified.

Corrective Actions Followin

Identification of the Failure to Perform Re uired

~Testin

After recognizing that the initial corrective actions failed to address the need to

periodically verify the time response

of the MFP turbine stop valves the licensee

initiated the following actions:

A POA was written to address the lack of response

time testing of the MFP

trip feature.

I

A TS interpretation 97-04 was issued which determined that MFP turbine

stop valve time response

testing should be included in TS.

AR A0433144

was written to track the actions needed to add this requirement to TSs.

STP V-3P7 was issued to perform the response

time testing of MFP turbine

stop valves on a refueling frequency.

Response

time testing was accomplished for both Units

1 and 2 MFP turbine

stop valves.

The inspector reviewed the corrective actions and determined that they appeared to

be appropriate

and if followed through would correct the discrepancies.

The licensee's failure to periodically verify the MFP turbine stop valves performed as

assumed

in the MSLB safety analysis is a violation of 10 CFR Part 50, Appendix B,

Criterion Xl, "Test Control."

This licensee-identified

and corrected violation is

being treated as a noncited violation; consistent with Section VII.B.1 of the NRC

Enforcement Policy (NCV 50-275;323/97006-07).

4

-27-

c.

Conclusions

The licensee's

response

following the identification of the need to response

time

test MFP turbine stop valves in September

1993 was untimely and failed to address

the identified testing discrepancy.

This problem is indicative of a previous lack of

attention to detail and deficient engineering

management

oversight and review of

corrective actions.

Detailed research

by an NQS engineer of past problems with MFP turbine stop

valves resulted in identification of the inappropriate

closure of AR A0316872.

This

is considered

to be noteworthy since these efforts resulted in the identification and

correction of a significant discrepancy.

E8.2

Chan

es Included in Revision

11 to the UFSAR Without Safet

Evaluations

a.

Ins ection Sco

e

37551

The inspector reviewed changes that were included in Revision

11 to the UFSAR

without having completed safety evaluations

in accordance

with 10 CFR 50.59.

The following FSAR Update change

requests,

which were included in Revision 11

were reviewed:

Sections 3.3, 5.1, 5.2, 5.4, 5.5, 5.6.2, 8.1, 8.2, 8.3, 9.5.2, 9.5.3,

and 9.3.

b.

Observations

and Findin s

The changes that were made to the UFSAR were reviewed by the inspector.

The

majority of the changes

appeared to be editorial or provide clarification to the

UFSAR for agreement with existing plant conditions and/or the associated

design

criteria memorandum.

None of the changes

appeared

to involve physical changes

to the plant and had originally been determined by the licensee not to require formal

safety evaluations.

However, these changes

did warrant safety evaluations to

determine whether or not they involved unreviewed safety questions.

The licensee

issued Revision

11 to the UFSAR in November 1996, which included these

changes,

without having completed the associated

safety evaluations.

The safety

evaluations for these changes

were not completed until approximately 6 months

later.

c,

Conclusions

The failure to perform safety evaluations when required by procedure prior to

implementation of the changes

in the UFSAR will be reviewed as a part of the

unresolved

item tracking UFSAR discrepancies

(URI 50-275;323/96006-06).

-28-

IV. Plant Su

ort

R1

Radiological Protection and Chemistry Controls

R1.1

Radiolo ical Controls Durin

the H drolasin

of Unit 2 Lower Reactor Cavit

a.

Ins ection Sco

e 71750

The inspectors reviewed the events leading up to, and the licensee's

response

following, the spread of radioactive contamination

in the FHB during the hydrolasing

of the Unit

1 lower reactor cavity.

The following documents

were reviewed:

Procedure

OP B-2:Vl, Revision 12, RHR - Draining the Refueling Cavity

Procedure

MP M-19.3, Revision 7, Fuel Transfer Tube Cover Removal and

Installation

Radiation Control Procedure

D-661, Revision 5, Decontamination of the

Reactor Cavity by Strippable Coatings

Procedure

OP L-6, Revision 26A, Refueling

Contamination Surveys 97-03912 and 03913, Unit 1 FHB (South)

AR A0434161, Spread of Significant Contamination Outside of. a Surface

Contamination Area (SCA)

b.

Observations

and Findin s

Events Resultin

in the S read of Contamination

On May 20, 1997, RP personnel

performed hydrolasing to decontaminate

the lower

reactor cavity surfaces.

Prior to commencing the hydrolasing,

RP personnel

had

contacted the Unit 1 control room to determine the status of the spent fuel

pool (SFP) transfer tube Valve SFS-50.

Operations personnel

relied upon an

abnormal status board to verify that Valve SFS-50 was closed.

RP was concerned

about the position of the valve since, if open, it provided a direct

pathway from the lower reactor cavity into the FHB. This was undesirable

since it

created the potential for the spread of contamination into the FHB during

hydrolasing.

Hydrolasing conducted

during a previous outage with Valve SFS-50

open had resulted in the spread of contamination

in the FHB.

Following the hydrolasing, an operator exiting the Auxiliary Building radiologically

controlled area alarmed the personnel contamination monitor.

Surveys showed

contamination levels as high as 3,500 counts per minute (cpm) on the operator's

-29-

shoes,

right upper arm and chest areas of his shirt.

RP investigation of the

contamination identified the spread of loose contamination adjacent to the Unit

1

SFP in the FHB. Subsequently,

it was determined that Valve SFS-50 was open

during the hydrolasing.

Contamination

Levels in the FHB

Surveys of the FHB showed contamination

levels of up to 30,000 cpm on large area

swipes.

Contamination was noted outside SCAs primarily in the areas adjacent to

the SFP with the highest levels being adjacent to the fuel transfer canal.

Survey

results showed contamination levels as high as 10,000 disintegrations

per minute

per 100 cm'

RP personnel

subsequently

decontaminated

the areas outside of the

SCAs to restore normal access to the FHB. The inspector noted that the levels of

contamination found during the surveys were not wide spread

and did not create

a

significant radiological hazard to workers who entered the area.

Procedural Controls for Refuelin

Procedure

OP L-6 provides the sequence

and procedures that are performed in

support of refueling.

Procedure

OP L-6, among other things', sequences

the draining

of the lower reactor cavity and the closing of Valve SFS-50.

Specifically,

Step 6.3.6 directs the'draining of the lower reactor cavity and transfer canal

utilizing Procedure

OP B-7:Vll, which opens Valve SFS-50.

Procedure

OP L-6,

Step 6.3.7, directs that Valve SFS-50 be closed when the spent fuel pool side of

the transfer canal is fully drained.

Hydrolasing was conducted after completion of

draining the lower reactor cavity and transfer canal, but prior to closing

Valve SFS-50.

Procedure

OP L-6 does not address the sequencing

of hydrolasing

activities in the lower reactor cavity.

Prior to the draindown of the cavity and transfer canal, operators

had hung a

clearance

(for the installation of the fuel transfer tube cover) which closed

Valve SFS-50.

Since Valve SFS-50 was required to be open for the draindown,

operators

had to remove the clearance

on Valve SFS-50 in order to accomplish the

draindown.

Following completion of the draindown, when RP personnel

called the

control room to determine the position of Valve SFS-50, the operator assumed that

the valve was shut since he had hung the clearance

on the valve earlier in the shift.

Additionally, the control room status board incorrectly showed Valve SFS-50 to be

closed.

Operations did not require a clearance to ensure that Valve SFS-50

remained closed for hydrolasing.

The licensee indicated that they planned to use a

clearance to assure that Valve SFS-50 is closed prior to future hydrolasing activities

in the reactor cavity.

Conclusions

Operations failed to establish positive controls to ensure Valve SFS-.50 was closed

during hydrolasing.

As a result, due to the combination of an incorrect control room

-30-

status board and inadequate

verification of Valve SFS-50 valve position, hydrolasing

was conducted with Valve SFS-50 open, which resulted in the spread of

contamination into the FHB.

V. IVlana ement Meetin

s

X1

Exit Meeting Summary

The inspectors presented

the inspection results to members of licensee management

at the

conclusion of the inspection on June 5, 1997.

A separate

exit meeting was held for the

control room observations

of Section 01.8 on May 22, 1997.

In both meetings the

licensee acknowledged

the findings presented.

The inspectors asked the licensee whether any materials examined during the inspection

should be considered

proprietary.

No proprietary information was identified.

ATTACHMENT

PARTIAL LIST OF PERSONS CONTACTED

Licensee

J. R. Becker, Director, Operations

W. G. Crockett, Manager, Nuclear Quality Services

T. L. Grebel, Director, Regulatory Services

T. F. Fetterman,

Director, Instrumentation

and Control Engineering

S. R. Fridley, Manager, Outage Services

D. J. Hampshire, Senior Engineer,

Balance of Plant Engineering

S. C. Ketelsen, Senior Engineer, Regulatory Services

D. B. Miklush, Manager, Engineering Services

J. E. Molden, Manager, Operations Services

D. H. Oatley, Manager, Maintenance

Services

R. P. Powers, Manager, Vice President

DCPP and Plant Manager

J. A. Shoulders,

Director, Support Engineering

D. A. Taggart, Director, Nuclear Quality Services Engineering

and Procurement

R. L. Thierry, Director, Balance of Plant Systems

R. A. Waltos, Director, Engineering Services

INSPECTION PROCEDURES USED

IP 37551: Onsite Engineering

'P

40500: Effectiveness of Licensee Controls in Identifying, Resolving and Preventing

Problems

IP 61726: Surveillance Observations

IP 62707: Maintenance

Observations

IP 71707: Plant Operations

IP 71750: Plant Support

IP 92901: Followup - Plant Operations

IP 92902: Followup - Maintenance

IP 92903: Followup - Engineering

ITEMS OPENED, CLOSED, AND DISCUSSED

~Oened

50-323/97006-0.1

VIO

Failure to maintain an operator-at-the-controls

as

required by procedure

-2-

50-323/97006-02

50-323/97006-03

VIO

Failure to properly install Sl breaker cubicle fasteners

NCV

Inadequate

procedure for installation of power supply to

sealer/timer audio count rate

50-275;323/97006-04

NCV

Failure to perform ASME required ISls

50.-275;323/97006-05

50-275/97006-06

IFI

Slow response

to industry information

VIO

Failure to assure spray shields enclose

RCP liftoil pump

lines

50-275;323/97006-07

NCV

Failure to time response test MFP turbine stop valves

Closed

50-323/96004-00

LER

Fuel movement not suspended

when source range

audible indication stopped

50-323/97006-03

NCV

Inadequate

procedure for installation of power supply to

sealer/timer audio count rate

50-275/83040-00

LER

Missed ISI surveillance

50-275;323/97006-04

NCV

Failure to perform ASME required ISls

50-275;323/97006-07

NCV

Failure to time response test MFP turbine stop valves

Discussed

50-275;323/96006-06

URI

Failure to adequately review and update the FSAR

1

LIST OF ACRONYMS USED

AR

ASME

CFCU

CPM

CVCS

CO

DCPP

FHB

FSAR

IFI

IN

ISI

ISEG

LER

kv

MFP

MFW

MP

NCV

NQS

OP

POA

PDR

PSIG

PSRC

POA

RCP

RHR

RP

SCA

SCO

SFP

SFM

SG

SI

STP

TS

UFSAR

URI

1R7

1RS

2R7

2RS

inspection followup item

Information Notice

inservice inspection

Independent

Safety Engineering

Licensee Event Report

kilovolt

main feedwater pump

main feedwater

Maintenance

Procedure

noncited violation

nuclear quality services

Operations

Procedure

prompt operability assessment

Group

Public Document Room

pounds per square inch gage

Plant Staff Review Committee

prompt operability assessment

reactor coolant pump

residual heat removal

radiation protection

surface contamination

area

senior control operator

spent fuel pool

shift foreman

steam generator

safety injection

surveillance test procedure

Technical Specification

Updated Final Safety Analysis Report

unresolved item

Unit 1 seventh refueling

Unit 1 eighth refueling

Unit 2 seventh refueling

Unit 2 eighth refueling

action request

American Society of Mechanical Engineers

containment fan cooler unit

counts per minute

chemical and volume control system

control operator

Diablo Canyon Power Plant

~

fuel handling building

final safety analysis report

l>>