ML16342D764

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Insp Repts 50-275/97-10 & 50-323/97-10 on 970608-0719. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support
ML16342D764
Person / Time
Site: Diablo Canyon  
Issue date: 08/08/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML16342D763 List:
References
50-275-97-10, 50-323-97-10, NUDOCS 9708190259
Download: ML16342D764 (48)


See also: IR 05000275/1997010

Text

ENCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket Nos.:

License Nos.:

Report No.:

Licensee:

Facility:

Location:

Dates:

Inspectors:

50-275

50-323

DPR-80

DPR-82

50-275/97-1 0

50-323/97-10

Pacific Gas and Electric Company

Diablo Canyon Nuclear Power Plant, Units

1 and 2

7 1/2 miles NW of Avila Beach

Avila Beach, California

June 8 through July 19, 1997

M. Tschiltz, Senior Resident Inspector

D. Allen, Resident Inspector

B. OIson, Project inspector

W. Ang, Reactor Inspector

Approved By:

H. Worg, Chief, Reactor Projects Branch

E

ATTACHMENT:

Supplemental

Information

970829'025'P

970808

PDR

ADOCK 05000275

8

PDR

EXECUTIVE SUMMARy

Diablo Canyon Nuclear Power Plant, Units

1 and 2

NRC Inspection Report 50-275/97-10; 50-323/97-10

~Oerations

Control room operator's actions in response

to the condensate/feedwater

transient

and subsequent

Unit 2 trip on July 2 were timely and appeared

to mitigate the

effect of the toss of both main feedwater pumps (MFPs) on other plant parameters.

The evaluation of the event and plant response

was thorough.

Subsequent

corrective actions taken to improve the unit's ability to w'ithstand similar transients

were based upon

a thorough investigation of the event.

The subsequent

power

ascension

was cautious and involved several verifications of condensate

and

feedwater system operation prior to returning to 'IOO percent power (Section 01.2).

I

O

A violation was identified when inspectors noted that the licensee's procedures for

alignment of a vital 480V power source to an instrument panel had not been

followed during the restoration from maintenance

that deenergized

the normal

power supply to the panel. Walkdowns of the power supply alignment verified that

normal power had been properly aligned; however,

a sealed component checklist

had not been completed for the transfer switch and the backup power supply

breaker was not positioned in accordance

with procedural requirements

(Section 01.4).

Maintenance

Postmodification testing for replacement of engineered

safety feature timers for

Containment

Fan Cooler Unit (CFCU) 2-3 was thorough and demonstrated

the

acceptable

performance of the design change.

The test participants performed the

test cautiously, with good coordination with operations

(Section M1.1).

Good test coordination occurred between reactor engineering

and operations

during

performance of Nuclear Power Range Incore/Excore Multiple-point Calibration

surveillance.

Additionally, the control operator made good use of plant process

computer to monitor plant parameters

and control core reactivity to obtain accurate

data in support of the test (Section M1.2).

A violation eras identified involving a containment isolation valve in an instrument

line that was not included in the monthly surveillance and had not been verified

closed at least once per 31 days (Section M1.3).

(

A noncited violation was identified when the licensee noted that Mode 3 had been

entered with an inoperable centrifugal charging pump (CCP)

~

CCP 1-1 was

determined to have been inoperable,

due to total pump flow in excess of that

allowed by Technical Specifications

(TSs), as a result of erosion of the miniflow

restriction orifice (Section M8.1).

-2-

Review'of the licensee's

control of RTV-732 caulking material revealed that the

licensee allowed its use in containment without administrative controls.

Tests of

the RTV-732 sealant conducted

by the licensee demonstrated

that the sealant was

not qualified for use in a harsh environment (Section M8.2).

~

Temporary modification/Jumper 97-017, which installed instrumentation

and

recorders to assist in troubleshooting

the cause of the July 2 trip, was well planned

and properly implemented.

However, the inspectors

noted several errors in the

documentation

of the jumper indicating a lack of attention to detail (Section 01.3).

~En ineerin

~

The design change for the replacement of the CFCU engineered

safety feature

timers effectively coordinated

the activities from initial design planning to final

implementation.

Cross-discipline engineering reviews, probabilistic risk analysis

assessment

and a licensing basis impact evaluation (LBIE) evaluation were

appropriately performed.

Affected procedures

and drawings were identified and

revised (Section E1.2) ~

In the control room several drawings and schematics

issued by engineering were

noted to have portions that were illegible. After identifying this situation to the

licensee,

an extensive review was performed which identified numerous drawings

and schematics that also had portions that were illegible.

Based upon the number

of discrepancies

noted, the inspectors concluded that the licensee's

program for

maintaining drawings and schematics

in the control room tailed to ensure that the

drawings were legible (Section 01.1).

Plant Su

ort

o

During the performance of the reactor coolant sample, the chemistry technician was

noted to be knowledgeable

of primary sampling procedures,

equipment use, and

radiological controls.

Primary samples were obtained satisfactorily (Section R4.1).

Re ort Details

Summar

of Plant Status

Unit

1 began this inspection period at 100 percent power.

The unit remained at

100 percent power throughout the inspection period.

Unit 2 began this inspection period at 100 percent power.

On July 2, the unit was

manually tripped by control room operators when a loss of suction pressure to the MFPs

resulted in the pumps tripping on overspeed.

The unit was returned to 100 percent power

on July 10.

Unit 2 completed the inspection period at 100 percent power.

I. 0 erations

01

Conduct of Operations

01.1

General Comments

71707

Using Inspection Procedure 71707, the inspectors conducted frequent reviews of

ongoing plant operations.

In general, the conduct of operations was professional

and safety conscious.

Review of drawings and schematics

issued by engineering

in the,control room

revealed that on some drawings there were areas which were illegible. After

inspectors

raised the concern, the licensee performed

a review of all control room

drawings and schematics.

The review identified numerous drawings and

schematics that had portions that were illegible and needed

replacem

nt. The

licensee issued

an action request

(AR) to document the problem and initiated

actions to replace drawings that were not completely legible. The inspectors found

that the actions taken by the licensee were responsive to the concerns.

Based upon the number of discrepancies

noted the inspectors concluded that the

licensee's

program for maintaining up-to-date drawings in the control room failed to

ensure that the drawings were completely legible.

01.2

Unit 2 Manual Reactor Tri

on Loss of MFPs

a.

Ins ection Sco

e 71707

On July 2, at 4:56 a.m. PDT, Unit 2 operators initiated a manual reactor trip after

the overspeed

trip of both MFPs.

The plant response

after the trip was

unccmplicated.

The inspectors reviewed the operator's

response

to the event, the

investigation of the cause,

and corrective actions prior to the return to power.

b.

Observations

and Findin

s

Unit 2 was at 100 percent power when operators observed

a decrease

in generator

output, followed by indications of loss of

uction pressure to the MFPs.

The speed

of both MFPs inc-eased

in response

to <he decreased

flow to tl e steam generators

-2-

and the MFPs tripped on overspeed.

The operators

responded

to the secondary

plant transient by decreasing

reactor power and manually tripped the reactor when

the MFPs tripped.

The unit was stabilized in Mode 3 with the reactor coolant

system

(RCS) at normal no-load temperature

and normal operating pressure.

Emergency

Diesel Generator

(EDG) 2-2 had started on the electrical power transfer

from auxiliary power to startup power (as had occurred

in past reactor trips).

Main

Feedwater

Regulating Valve 2-2 had shifted to manual during the transient (due to

controller setpoints for limiting plant response

to out-of-range parameters).

Soth of

these automatic actions were considered to be expected responses

to the transient.

The licensee developed

a plan to evaluate the cause of the loss of suction pressure

to the MFPs, reviewed the plant response

to the transient, evaluated the EDG and

main feedwater regulating valve response,

and implemented their 2-day outage plan.

The review of the transient identified that the interaction of several control valves in

the condensate

system, and their associated

controllers, caused the flow to the

suction of the MFPs to decrease

below that required to maintain adequate

feedwater flow to the steam generators.

A recent throttling of a manual valve in

parallel with these control valves is believed to have contributed to the plant's

inability to recover from this condensate

flow transient.

The licensee fully opened

.

the manual valve and adjusted the controllers for the control valves to slow the

valve response

to system transients.

The unit was returned to power operation,

with holdpoints at several power levels to obtain condensate,

and feedwater system

data and evaluate the plant's response to normal steady state conditions and

planned transients.

The evaluation of the trip indicated that the initiating event was a sudden

loss of

condenser

vacuum.

The licensee identified all known causes for a loss of vacuum

and by review of recorder", inspection of equipment,

and questioning of personnel

eliminated each as the initiator for this plant trip. After the initial loss of vacuum,

the response

of other plant parameters

and equipment operation appeared to have

been adequately

evaluated.

Conclusions

The operators

actions in response

to the transient and subsequent

unit trip

mitigated the effect of the loss of both MFPs on other plant parameters.

The

licensee performed an exhaustive evaluation of the trip and the plant response.

Although the initiating cause for the loss of vacuum had not been identified,

corrective actions were taken to improve the unit's ability to withstand

a similar

transient without a plant trip. The corrective actions have also been implemented

in

Unit 1 where applicable.

The subsequent

return to power was performed cautiously

with prudent testing and adjustments

made at appropriate power levels.

~

~

-3-

01.3

Review of Tem orar

Modifications Jum

er Lo

a.

Ins ection Sco

e 71707

'The inspectors reviewed the jumper log and walked down the jumpers (Unit 2

Jumper Log 97-017) associated

with monitoring the condensate

system parameters

in troubleshooting

the cause of the Unit 2 trip on July 2.

The applicable

Administrative Procedure,

CF4.ID7, "Temporary Modifications - Plant Jumpers

and

M8cTE", Revision 5, was also reviewed.

b.

Observations

and Findin

s

The jumpers did not result in inoperability of safety-related

equipment and had

appropriate

evaluations

and actions implemented.

No conflicts with TS or the

Updated Final Safety Analysis Report were identified.

The jumpers and

instrumentation

associated

with the condensate

system monitoring were installed as

described on the jumper log, with adequate

restraints to prevent becoming

a hazard

to plant equipment.

A combustible loading permit had been obtained and was

located at the job site.

Information tags were attached to the jumpers as required

by the administrative procedure.

Data f.om the instrumentation

divas being recorded

periodically and the strip charts were routinely collected and evaluated.

The jumper

Iog was reviewed and contained the necessary

information, licensing basis impact

screening,

and approvals

as required by the administrative procedure.

Several

administrative errors were noted in the jumper log including:

an error in annotating

the screening for the LBIE; inappropriate

line out of the signatures for installation

and verification of two jumpers; and an attached drawing had an incorrect markup.

These administrative discrepancies

were identified to the licensee

and were

corrected.

c.

Conclusions

The temporary modification for monitoring the condensate

system after the July 2

transient had been adequately

planned

and reviewed, and the jumpers were properly

installed as described

in the jumper Iog.

In general, the jumper logs were properly

maintained.

The errors noted in Jumper Log 97-017 indicated

a lack of attention to

detail and failed to meet management

expectations.

01.4

Walkdown of Unit

1 480V Switch ear

a ~

Ins ection Sco

e 71707

The inspector performed

a routine walkdown of the Unit

1 480 volt switchgear on

July 1, 1997, and reviewed the following procedures:

~

OP J-10:IV, Revision 19, Instrument AC System

- Transfer of Panel

Power Supply

~

Switching Order dated 5/24/97

OP 0-13, Revision 9, Transferring Equipment to/from Alternate Power

Source

~

OP1. DC20, Revision 6, Sealed Components

b.

Observations

and findin s

During a walkdown of the Unit 1 480V Bus F,switchgear, the inspector noted that

Breaker 52-1F-27 was closed, although it's normal position is open.

The breaker

supplies backup power to 120V instrument Panels PY-15, PY-16, and PY-17.

PY-

15 and PY-16 are normally powered from the vital 480V Busses

G and H,

respectively, while PY-17 is normally powered from a nonvital 480 volt bus.

Procedure

OP J-10:IV, Section 6.21, specifies the procedure for transfer of PY-16

from backup to normal power.

Procedure

OP J-10:IV, Step 6.21.4, requires that

the backup 480V supply Breaker 52-1F-27 be opened following realignment of the

normal power supply.

Additionally, Note

'l in Section 6.21 specifies that the use of

a transfer change form per OP1.DC20 is required.

Procedure

OP1.DC20,

paragraph 4.2.6 requires that removal and replacement

of seals shall be

documented

and that a transfer switch change form shall be issued and approved

prior to the component seals being broken.

Following completion of the sealed

component

change form it is required to be filed in the control room.

During

1 R8, the 480V Bus G was deenergized

to perform inspections of 4 kV

breakers.

During the time that Bus G was deenergized,

the power supplying PY-16

was realigned to its alternate power source.

Following completion of the

maintenance,

after reenergizing

Bus G, the licensee aligned the normal power supply

to PY-16.

During the restoration, breaker 52-1F-27 was left closed contrary to

procedural requirements.

Additionally, there was no record of the removal and

reinstallation of the seal installed on the power transfer switch, contrary to

procedural requirements.

A walkdown of the other power supplies was performed and revealed that all three

of the PY panels were powered from their normal power supply.

Breaker 52-1F-27

being closed and out of its normal position did not adversely impact the operability

of any components

since the normal power supplies were properly aligned;

however, the lack of documentation

and the fact that breaker 52-1F-27 was not

properly restored to the open position, indicated that applicable procedures

were not

followed when performing the restoration of normal power to the instrument panel.

The failure to follow procedures

for sealed components

and for realignment of

instrument Panel PY-16 is a violation of 10 CFR Part 50, Appendix B, Criterion V

(VIO 50-275/971 C-01).

-5-

c.

Concl'ions

Operators failed to follow procedures

for aligning 480 vital power to instrument

Panel PY-16.

08

Miscellaneous Operations Issues (92700)

08.1

Closed

Licensee Event Re ort

LER 50-275 95014 Revision 0: diesel generators

started and loaded as designed

upon failure of Auxiliary Transformer

1-1 due to

inadequate/ineffective

procedures

relating to the control of grounding devices.

e

This LER was written to document the loss of all offsite power following the failure

of Auxiliary Transformer 1-1 while the startup bus was deenergized

for

'maintenance'.

Following this event the NRC conducted

a special inspection, the

results of which are documented

in NRC Inspection Report 50-275;323/95-017.

Following review of the LER, the inspector determined that no new violations were

documented

and that the violations issued in the inspection report documented

the

pertinent issues pertaining to the event.

The associated

corrective actions for this

event are documented

in the response

to the violations and the NRC's review and

closure of the violations, therefore, no additional review is necessary to close this.

LER.

II. Maintenance

IVI1

Conduct of Maintenance

M1.1

Maintenance

Observations

ine ection Sco

e (~62707

The inspectors observed

all or portions of the following work activities:

C0152981

Remove and replace TM-3 and POT-32 components

in the

TCV-23 control circuitry

R0162375

Inspect auxiliary saltwater (ASW) Pump 1-'I vault drain line

check Valve SW-1-987

M1.2

CFCU Timer Re lacement Postmodification Testin

a.

Ins ection Sco

e 62707

'he inspectors observed

portions of postmodification Procedure PMT-23.26,

"CFCU 2-3 Time Delay Relays Replacement Test", Revision 0.

-6-

Observations

and Findings

The Design Control and Test Group performed the postrnodification test for the

replacement of the auto transfer timer and safety injection (Sl) timer for CFCU 2-3,

in accordance

with Procedure PMT-23.26.

The initial section of the procedure

tested the control circuit while electrically isolated from the motor electrical power.

This allowed a thorough checkout of the interlocks and seal-in paths without undue

cycling of the CFCU.

Later sections of the procedure

simulated autotransfer

signals

and Sl signals to the control logic and verified by actual operation of the CFCU that

the design modification had been properly designed

and implemented.

The test briefings covered the necessary

information (including test conditions,

organizational interfaces, test requisites, expected

alarms, expected component

changes

of state, ar.d test connections)

and the operators

and other test

participants clearly understood

their tasks and responsibilities.

The instrumentation

was within calibration and appropriate for the test.

Electrical safety precautions

were used when connecting

and disconnecting

from energized equipment.

Three-way communications

were used by the operators and test personnel.

Electrical schematic and connection drawings were available in the field and used to

ensure the actions in the procedure

and the plant response

were understood

before

proceeding.

The personnel performing the test were knowledgeable

of the equipment operation

and the intent of the design change.

The test procedure was performed and signed

as written, with-several minor on-the-spot-changes

(OTSC).

One OTSC was due to

the procedure

specifying incorrect fuse ratings.

Another was due to a procedure

error that verified a rel.y deenergized

when in fact it did not change state.

Both of

these errors should have been noted and corrected prior to starting the test by a

review of the tests performed on the Unit 1 CFCUs.

During the autotransfer part of the test, CFCU 2-5 was expected to stop and restart

in slow speed; however, it initially remained running in fast speed

and then shifted

to slow speed.

The test personnel

and operators worked well together to stop the

test and return plant equipment

and test jumpers to a normal and safe configuration.

The response

of the CFCU was documented

in an AR and evaluated before

proceeding with the remainder of the test.

The evaluation concluded

CFCU 2-5 has

performed as designed.

Conclusions

The personnel were well prepared

and knowledgeable

about the test.

The test

demonstrated

the design modification had been implemented properly and satisfied

the intent of .he design change.

!n general, the procedure was thorough and

properly used.

Procedural deficiencies that required an OTSC should have been

identified prior to the start of the test from lesson learned from the Unit

1

-7-

performance of the equivalent tests.

Involved personnel

responded

cautiously and

appropriately to the unexpected

performance of CFCU 2-5.

M1.2

Surveillance Observations

Ins ection Sco

e 61726

Selected surveillance tests required to be performed by TS were reviewed on a

sampling basis to verify that:

(1) the surveillance tests were correctly included on

the facility schedule;

(2) a technically adequate

procedure

existed for the

performance of,the surveillance tests; (3) the surveillance tests had been performed

at a frequency specified in the TS; and (4) test results satisfied acceptance

criteria

or were properly dispositioned.

The inspectors observed

all or portions of the following surveillances:

STP R-13

Nuclear Power Range Incore/Excore Multiple-Point Calibration,

Revision 98

STP R-41

STP M-9A

RCS Temperature

Instrumentation

Data, Revision 6

Diesel Engine Generator Routine Surveillance Test,

Revision 43A

b.

Observations

and Findin s

During the performance of STP R-13, the shift foreman, shift technical advisor and

reactor engineering

provided good support for the evolution.

The reactor engineers

clearly communicated the necessary

plant conditions for data collection and the

control operator made good use of the plant process computer and its displays to

monitor and control plant parameters

critical to obtaining high quality data for the

test.

c.

Conclusions

The inspectors found that the surveillances

observed were being scheduled

and

performed at the required frequency.

The procedures

governing the surveillance

tests were technically adequate

and personnel performing the surveillance

demonstrated

an adequate

level of knowledge.

The inspectors noted that test

results appeared

to have been appropriately dispositioned.

-8-

M1.3

Surveillance

Re uirements for Containment

Isolation Valve SI-1-8964

lns ection Sco

e 61726

The inspectors reviewed STP I-1D, "Routine Monthly Checks Required By Licenses",

Revision 48, for compliance with TS 4.6.1.1.a, whicl; requires containment isolation

valves to be verified closed every 31 days.

b.

Observations

and Findings

The operating valve identification diagram for the Sl system shows containment

Penetration

518 with a line used to test check valve leakage and to fillthe Sl

accumulators.

A branch of this line, outside containment,

has

a pressure

Indicator,

1-PI-942, with a normally closed manual isolation Valve, Sl-1-8964.

Valve Sl-1-

8964 is therefore part of the containment isolation barrier for a penetration that is

required to be closed during accident conditions and should be verified to be in its

closed position at least once per 31 days as required by containment integrity TS

Surveillance Requirement 4.6.1.1.a.

This valve was not verified as part of STP I-1D

and was not verified closed every 31 days.

The licensee was informed and the

operating crew verified the valves on both units to be closed.

The licensee's

position was that this valve is not a containment isolation valve and

was not within the scope of Surveillance Requirement (SR) 4.6.1,1.a.

Containment

isolation valves operability is covered by TS 3/4.6.3 which clearly applies to active

valves.

The action statement for an inoperable isolation valve includes isolating the

affected penetration

by use of a deactivated

automatic valve secured

in the isolation

position, or isolation by use of a closed manual valve or blind flange.

The

surveillance requirement for containment integrity, SR 4.6.1.1.a, addresses

penetrations

not capable of being closed by an operable containment automatic

isolation valve, and verifying closed valves, blind flanges, or deactivated automatic

valves secured

in their positions, except for valves that are open under

administrative controls as permitted by TS 3.6.3.

The licensee believed that these

requirements

applied to main process valves only, and not to test vents and drains,

or to instrumentation valves that might form part of the containment penetration

boundary.

The local leak rate test valves were included in Procedure

STP I-1D

because

Standard

Review Plan, Section 6.2.6, requires test, vent, and drain

connections that are used to facilitate local leak rate testing or the performance of

the containment integrated leak rate test should be administratively controlled and

should be subject to periodic surveillance.

The NRC's TS Branch interpretation

is that any valve associated

with a coritainment

penetration,

no matter how small, is a containment isolation valve and the

requirements

of TS 3.6.1.1 apply.

-9-

Licensee's

Corrective Actions

'

Following discussions

with the NRC inspectors

and TSB, the licensee began

a

thorough review of the containment penetrations

to.identify any additional valves

that had not been included in Procedure

STP I-1D. The penetrations

to be reviewed

were prioritized, with those penetrations

most likely to have valves that were

excluded reviewed. first. Penetrations

which receive local leak rate testing were

reviewed last, since the valves associated

with them were already included in

Procedure

STP I-1D. The review also included valves inside containment, which are

excepted for the 31-day requirement of SR 4.6.1.1. if they are locked, sealed,

or

otherwise secured

in the closed position.

These valves inside containment

are

required to be verified closed during each cold shutdown except such verification

need not be performed more often than once per 92 days.

Those valves outside

containment

and accessible

valves inside containment that had not been verified

closed are being checked by operations

and verified closed, and where applicable,

downstream

pipe caps were verified to be in place.

Related Industr

Problems

In December 1992, Florida Power and Light Company was issued

a violation for

failure to maintain containment integrity by opening

a drain valve in the containment

spray system which was also a containment penetration boundary valve

(documented

in NRC Inspection Report 50-335;389/92-21).

The licensee stated

that they were not in TS 3.6.1.1 Action Statement

because

only valves identified

by number in the TS or the Updated Final Safety Analysis Report were containment

isolation valves.

The licensee specifically stated that vents, drain and test valves

were not within the scope of the TS 3.6.1.1.

The NRC Staff review concluded any

valve which isolates

a containment penetration,

no matter how small, is a

containment isolation valve and is required to be within the scope of TS 3.6.1.1.

In September

1996, NRC Reaion

II requested

NRR to evaluate

a Catawba site

document entitled "Catawba Nuclear Station Containment Integrity Review" for

consistence

with various regulations and cod'es.

The licensee's

document

contended

that ANSI N271-1976 clearly differentiated between test connection

vents and drains and containment isolation valves.

It further contended that the

Standard

Review Plan Sections 6.2.4 and 6.2.6 also distinguish between

containment isolation valves and test connections

vents and drains,

and, therefore,

do not consider test vent and drain connections to be containment isolation valves.

The staff's response

was that test vents and drains (TVDs) are containment

isolation valves (CIVs}. The fact that ANSI N271-1976 has

a definition for TVDs

does not mean the TVDs cannot also be CIVs. The staff's position was that the

TVDs should meet the 31-day SR 4.6.1.1.a for CIVs.

ln November 1996, the resident inspector for Braidwood Station requested

NRR's

assistance

in interpreting TS 3/4.6, "P:imary Containment"

SR 4.6.1.1.a on a vent

and drain valve on a SI test line local pressure

indicator.

The licensee believed that

-10-

SR 4.6.1."..a, which requires the licensee to verify that all penetrations

are secured

every 31 days, applies orMy to penetrations

that are not capable of being

automatically isolated.

They stated that because

the penetration attached to these

valves is capable of being closed by an operable containment automatic isolation

valve, SR 4.6.1.1.a does not apply to these drain and vent valves.

NRR's TS

Branch reviewed the request

and concluded that these drain and vent valves should

be included in the SR testing.

The staff considers

any valve associated

with a

containment penetration

no matter how small to be a CIV and therefore the

requirements of TS 3.6.1.1 apply to them.

Part of the basis for the applicable

general design criteria is that a single failure will not prevent or degrade containment

integrity.

C.

Conclusions

l

The licensee's implementation of TS SR 4.6.1.1.a was inadequate

in that it failed to

verify that Valve Sl-1(2)-8964 was closed at least once per 31 days.

This is a

violation of TSs (VIO 50-275;323/9710-02).

M8

IVliscellaneous Nlaintenance Issues (92700)

M8.1

Closed

LER 50-275 94-023-00:

TS 3.0.4 was not met when Unit 1 entered

Mode 3 on May 4, 1994 with CCP 1-1 inoperable.

CCP 1-1 was inoperable

because

the total pump flow was greater than the TS 4.5.2h.1(d) limit.

The excessive

CCP 1-1 flow was caused

by erosion of the CCP miniflow restricting

orifices and leakage through flow control bypass Valves 83878 and C. The

excessive

erosion of the restricting orifices is believed to have been caused

by

extended

use of the CCPs for normal charging.

The licensee's corrective actions

included verifying the current flow balance satisfies the TS requirements,

replacement of the restricting orifices and adding flow measurement

equipment

in

the mini-flow path, and the use of the positive displacement

pump as the normal

supply for charging flow. The equipment modifications were completed

in Unit 1

during the 1R8 outage, and are scheduled

to he implemented

in Unit 2 during the

2R8 outage.

The review of the LER by the inspector revealed

no new information.

This licensee-identified

and corrected violation is being treated as a noncited

violation, consistent with Section VII.B.1 of the NRC Enforcement

Policy (50-275/97010-03).

M8.2

Use of Dow Cornin

RTV-732 in Containment

a.

Ins ection Sco

e 92902

As documented

in NRC Inspection Report 50-275;323/97-06

the appropriateness

of

the use of RTV-732 sealant to fillin gaps between the base of the reactor coolant

pumps and the lubricating oil collection pans was questioned

by the inspectors.

The inspectors performed additional reviews of the actions taken by the licensee

following identification of this issue.

I

Observations

and Findin s

Following the initial identification of the concern, the licensee determined that

RTV-732 sealant had not been qualified for use in containment

and would be

replaced with a qualified caulking material.

Testing performed by the licensee

determined

under harsh environmental conditions, that could be encounter

d in

cer.ain areas of containment during accident conditions, that the RTV-732

ealant

material may not adhere to the surface that it had been applied.

A.search was

performed to'determine the work orders which specified the use,of the RTV-732

sealant stock code for work performed in containmerit.

This search identified that

the use of the RTV-732 sealant had been specified on the CFCU 2-2 fan housing.

The licensee subsequently

reviewed the calculation for debris clogging the

containment sump and determined that the additional caulking material, if

transported to the containment sump during an accident, would not significantly

reduce the margin to safety in the calculation for adequate

emergency core cooling

system suction from the sump.

8ased upon the remaining margin in the calculation

this conclusion appeared

reasonable.

A prompt operability assessment

was written

based upon this information.

The licensee's

assessment

was questioned

by the inspector, since the work order

search did not identify ail of the reactor coolant pump oil collection trays as having

had RTV-732 applied.

Further review by the licensee revealed that RTV-732 had

been available for use in the tool crib in containment during outages.

Specifically,

during 1RS, six tubes of RTV-732 sealant had been used in containment based upon

tool crib inventory records.

The licensee was unable to identify where the RTV-732

sealant had been used.

8ased upon the previous analysis, the inspector agreed

with the licensee's conclusion that this did not change the validity of the licensee's

initial conclusion regarding the potential for clogging the containment sump.

However, the use of unauthorized

material in containment

is being considered

as an

inspection folfowup item pending the licensee'eview

of the impact of RTV use

during the outage to assure environmental qualification requirements continue to be

met {IFI 50-275;323/9710-04).

Conclusions

The licensee's

initial assessment

of the effect of the use of RTV-732 sealant in

containment was incomplete in that it failed to identify the total quantity of the

sealant used and the locations where it had been applied.

-1 2-

III. En ineerin

El

Conduct of Engineering

E1.1

Calculation in Su

ort of Com onent Coolin

Water

CCW Flow Balance

37551)

The licensee identified an error in a calculation for the CCW system.

Calculation M-916 specified instructions to be incorporated into test

Procedure

STP V-13A, "CCW Flow Balancing", to establish the CFCU outlet valve

positions to maintain CCW system hydraulic flow balance.

The instructions

included a correction for a difference in elevation of pressure

indicators.

This

correction was subtracted

from the measured

values; however, the correction

should have been added.

The licensee performed

a prompt operability assessment

and concluded that the CCW and CFCU systems remained operable.

The licensee

indicated that both the calculation and the surveillance procedures

were being

revised to correct this error.

The surveillance procedure was reviewed by the inspector and an additional error in

correcting for elevation of the test pressure

indicators was identified.

The elevation

of each indicator was determined

in reference to the floor elevations which were

incorrectly specified in the procedure.

This was identified to the licensee for

incorpo.ation into the procedure

revision.

The operability assessment

and corrective

actions adequately

addressed

these errors.

E1.2

CFCU Auto Bus Transfer and Sl Timer Re lacement Desi

n Chan

e

a.

lns ection Sco

e 37551

rhe inspector reviewed the Design Change

Package

E-049344, Revision 1, and

Design Change Notice 1-EE-049355, Revision 1, to a sess the design control and

installation ot plant modification processes.

b.

Observations

and Findin s

Design Change

Package E-049344 replaces

all Unit 1 existing 10 CFCU timers

(5 Sl and 5 auto bus transfer timers) with more accurate digital Agastat DSC timers.

The wiring changes

use existing 42X relays as auxiliary relays to meet seismic

requirements

and facilitate installation, as well as change the CFCU start logic such

that an autotransfer signal will start the CFCU in slow speed regardless of the

High/Low speed switch position.

The design change was the result of Quality

Evaluation Q0010264, which identified the existing Agastat 7000 series auto bus

tiansfer timers drift outside the range allowed by TS.

The effect on plant operation was addressed

by the design change package,

including changes

to operating, surveillance and administrative procedures.

The

engineering

evaluations

included seismic and environmental considerations

as well

-1 3-

as electrical calculations for loading of the EDGs and dropout voltages of the timers.

The probabilistic risk assessment

concluded that the change would be beneficial

since it does not introduce any new failure modes and the new timers are more

reliable.

The design change package specified the functional tests to be performed and the

acceptance

crite'ria to be satisfied to demonstrate

the modification functions as

intended.

The design was reviewed by appropriate interface organizations,

including operations,

maintenance

and other engineering

disciplines.

An LBIE screen

was performed and determined the need for a LBiE. The LBIE was performed, but

was not properly annotated

as to whether an unreviewed safety question was

involved or whether a TS change was required.

It appeared

from the LBIE that

neither was involved.

The discrepancy was pointed out to the licensee and

corrected.

A Final Safety Analysis Report (FSAR) 'change was identified and the

FSAR Update change request was submitted.

Revisions to Design Criteria

Memorandum S-23, heating, ventilation and air condition, and S-63, 4KV Systems,

have been submitted but not yet incorporated.

Design Change Notice 1-EE-049355, Revision 'I, contained the installation

requirements to implement the above plant modification.

It specified the necessary

sequence

of installation and the system lineup, and identified the TS requirements

applicable during installation.

The postmodification/functional tests and applicable

acceptance

criteria were specified.

The associated

field change forms, were

reviewed and found to correct a "neak circuit, clarify instructions, allow use of new

wire or existing spare wire and to correct minor errors.

The identified procedure changes

were reviewed and found to have been

implemented.

Control room dra;vings were reviewed and contained thri applicable

cnarkups.

c ~

Conclusions

The desigr control process effectively coordirated the necessary

activities from the

initial design planning to final implementation.

Interfaces between various

organizations

were controlled to ensure supporting activities were completed to ful/y

implement the plant modification.

The number of field changes

was not excessive,

but does indicate improvement could be made in the planning of the installation.

The design change appeared

to accomplish its intended function.

E8

Miscellaneous Engineering Issues (92903)

ES."

Closed

IFI 50-275/96006-04:

licensee long-term corrective actions to improve

source range instrument reliability. The control console startup rate meter for

source range Inst-ument Nl-32 stuck on its bottom peg on several occasior.s.

The

licensee had previously identified that the source and intermediate rar.ge startup

rate meters were the wrong current range (-0.1 to 0.9 made verses the correct

-1 4-

range of -0.1 to 1.0 made) and were procuring replacements.

The wrong range

meters were calibrated and oerformed the required function, and therefore were

acceptable

until the new meters could be installed.

During 1R8 outage,

the startup

rate meters for source and intermediate instruments were replaced with new

meters.

The applicable calibration Procedure,

STP I-37-N46 NIS Comparator and

Rate N46/N37 Calibration, was performed and the meters were observed

prior to

startup to operate properly without sticking.

The Unit 2 meters are scheduled for

replacement

during the next refueling outaoe.

Closed

URI 50-275 323 96021-06:

ASW TS interpretation more restrictive than

TS.

The inspector reviewed the unresolved

item (JRI) that was written after noting that

the TS 3.7.4.1 ACTION statement,

as written, no longer specified the lowest

functional capability or performance

levels for the ASW system.

Current TS 3.7.4.1

Re uirements

The TS limiting condition for operation, requires two operable ASW trains, with an

ACTION statement that with only one ASW train operable the second train must be

restored to OPERABLE status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or be in HOT STANDBY within the

following 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in COLD SHUTDOWN within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.

Licensee TS 3.7.4.1 Inter retation

The TS interpretation 95-08, implemented by the licensee, imposed more restrictive

requirements for ASW pumps and CCW heat exchangers

in order to ensure that

adequate

equipment was available to prevent overheating the CCAV system.

Although this was different than originally stated in the FSAR, the licensee had

performed

a 10 CFR 50.59 evaluation and revised the FSAR to reflect the system

configuration requirements.

Issues identified durin

revious NRC ins ections

During the review of this issue, the inspector determined that the NRC had

reviewed related issues in a safety system fur ctional inspection

in Sanuary 1989

(see NRC Inspection Rreport 50-275/89-01) and later during the review of the LER

submitted by the licensee following the inspection

(LER 50-275/84-40, see NRC

Inspection Report 50-275;323/89-013).

Following these inspections,

the NRC

determined that the licensee had not adequately translated

plant system

configuration design assumptions

into procedures.

Consequently,

operating

procedures

or instructions did not provide adequate

guidance for system operation

under certain design basis conditions.

A recent review of the associated

procedures

determined that the licensee had completed revisions to the procedures

which

appeared

to provide adequate

guidance.

-1 5-

CCW S stem Desi

n Chan

e Raised Maximum Allowed Tem erature

The licensee recently issued

a design change which raised the design temperature

of the CCW system to allow a temperature

transient in the system to 140'F for a

period not to exceed

6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.

Based upon the increase

in the maximum allowable

system temperature,

the additional restrictions implemented by the TS interpretation

are no longer required; however, in order to ensure maximum heat removal

capability during emergencies

operators

are instructed to place a second CCW heat

exchanger

in service early in the emergency operating procedures.

Additionally, the

licensee has submitted

a license amendment,

based upon the new analysis, which

require"., only one ASW pump and one CCW heat exchanger,

as assumed

in the

safety analysis, in order to provide sufficient heat removal to mitigate a design basis

accident.

Based upon the analyses, this unresolved

item is closed.

E8.3

(Closed

Violation 50-323/96023-05:

failure to initiate an AR to address

loose

fasteners.

On November 19, 1996, during a routine tour of the Unit 2 480V vital

switchgear rooms, the resident inspectors identified a number of loose fasteners

associated

with the breaker front panels.

These findings were discussed with the

system engineer and the onsite mechanical engineer responsible for seismic

qualification and evaluation of plant equipment.

On Noverr,ber 22, 1996, the

system engineer provided the resident inspectors

a technical evaluation regarding

the seismic qualifications of the affected breaker panels with the observed

loose

fasteners

and resolved the resident inspectors'oncerns

regarding the impact of the

observed

loose fasteners.

However, the resident inspectors determined

that as of

December 2, 1996, an AR had not been initiated to address

and document the

quality problem associated

with the loose fasteners contrary to Procedure AD4.ID8,

Revision 1, "Identification and Resolution of Loose, Missing or Damaged Fasteners."

On February

14, 1997, the licensee responded'to

the Notice of Violation by means

gf PGSE letter DCL-97-024 and agreed with the violation.

The licensee stated that

the following corrective actions had been taken:

~

An AR was written to document the observed fastener deficiencies and the

corrective actions that were taken.

The system engineer was trained regarding the need to document quality

problems as required by Procedure AD4.1D8.

A case study was written and distributed to plant personnel to provide

lessons

learned regarding the event.

Electrical and instrumentation

and controls system engineers

were given

specific training regarding the requirements

of Procedure AD4.1D8.

During the current inspection period, the inspectors reviewed the licensee corrective

actions for the violation as stated in the licensee response.

The inspectors

determined the following:

-1 6-

The licensee issued AR AO418696 on December 3, 1996, to document the

observed

loose fast. ners and the. corrective actions for'the fasteners.

The

'R

also addressed

the procedure violation regarding the failure to write the

AR.

AR AO4'l8696 also documented

the preparation

and issuance of a case

study regarding the violation on February 28, 1997.

The inspectors

reviewed case study 63 dated February 27, 1997, regarding the violation.

The inspectors noted that the case study provided a good description of,:he

problems identified and lesson learned.

The case study appropriately

discussed

the need to comply with procedural requirements

and the need to

document identified fastener problems.

AR AO418696 also documented

the completion of training of all electrical

and instrumentation

and controls system engineers

on March 21, 1997.

The

inspectors discussed

the training with the original system engineer involved

with the problem.

The inspectors noted that the system engineer was also

the individual who prepared the case study and was now fully aware of the

procedural requirement associated

with documenting fastener problems.

The inspectors concluded that the licensee had performed reasonable

corrective

actions for the identified violation. Additional problems noted with the control of

4 kV breakers werc documented

in a violation (VIO 50-275;323/97-06-02).

Corrective actions for those specific instances will be evaluated

during the review of

the licensee's

response

to the violation and willconsider the adequacy of the

ccrrective actions for previous similar violations.

Based on the above,

Violation 50-323/96023-05

was closed.

IV. Plant Su

ort

R4

Staff Knowledge and Performance

in Radiological Protection and'Chemistry Controls

R4.1

Primar

Coolant Sam

le Procedure

a.

Ins ection Sco

e l71750

On June 12, the inspector observed the drawing of RCS daily samples at Units

1

and 2 primary sample sinks.

Procedure

CAP E-', Revision 17A, "Sampling cf

Primary Systems," was also reviewed.

b.

Observations

and Findin s

The chemistry technician was knowledgeable

of the sampling procedure

and the

configuration and operation of valves at the primary sample sinks.

The chemistry

technician was sensitive to potent)ally contaminated

areas

and demonstrated

proper

f

-1 7-

radiological controls while working in the sample sink. A sufficient volume of

coolant was purged through the sample lines to ensure that representative

samples

were drawn.

The inspector verified that the" issued-for-use"

copy of Procedure

CAP E-1 located

in the primary sample room for each unit was the latest revision.

After the samples

were drawn, the inspector observed

portions of the sample analysis.

The inspector

observed that the chemistry technician was knowledgeable

of the required analysis

and use of the analytical equipment.

C.

Conclusions

The primary samples were obtained satisfactorily.

The chemistry technician was

knowledgeable

of the sampling procedure,

equipm'ent use, and radiological controls.

P1

Conduct of Emergency Preparedness

Activities

P1.1

Licensee

Pre

a'redness

for Criticalit Accidents

a.

lns ection Sco

e 71750

The inspectors

examined the implementation of 10 CFR 70.24, "Criticality Accident

Requirements."

b.

Observations

and Findin s

The licensee did not have an exemption from the requirements

of 10 CFR 70.24 in

the operating license.

However, on April 3, 1997, the licensee submitted a request

fear exemption from the requirements

of 10 CFR 70.24.

Currently, the licensee has

procedures

and equipment in place that appear to meet the requirements

of

10 CFR 70.24.

The inspectors verified that Diablo Canyon has two area radiation monitors

positioned near the fuel storage

and handling areas which are intended for the

monitoring of potential criticality events.

Area Radiation Monitor (RM)-59 was

positioned near the new fuel storage vault and area RM-58 was positioned near the

'pent fuel pool.

ln addition, licensee procedures

specified the placement of portable

criticality monitors near the new fuel storage vault and cask washdown areas,

as

applicable, during fuel handling activities.

Licensee personnel indicated that the

radiation monitors were capable of meeting the requirements

of 10 CFR 70.24(a)(1).

The monitors energized

local audible alarm signals if setpoints

are reached,

and

RM-58 and RM-59 energize control room annunciators

upon alarm.

The alarm response

procedures

for the remote alarm feature in the control room

have instructions that speci-y the actions to be taken and the requirements

for

initiating the emergency response

plan.

The actions include the evacuation

of

A

-18-

personnel from the fuel handling areas.

Procedure

OP B-SH, "Nonrefueling Fuel

Handling Instructions," also specifies the actions to be taken if any of the criticality

monitors alarm.

Licensee procedures

specify the performance of an on-station evacuation drill prior

to receiving fuel for each operating cycle.

Licensee procedures

also specify preshift

briefings of actions to be taken in the event of a radiation alarm or portable

criticality monitor alarm.

Conclusions

The licensee currently meets the requirements

of 10 CFR 70.24 for criticality

accidents.

PS

Miscellaneous Security and Safeguards

Issues (92904)

P8.1

Closed

Violation 50-275 9103-04:

inattentiveness

to duties.

This violation was issued after a security officer, assigned

as a compensatory

measure watch, was observed to be inattentive.

The licensee acknowledged

the

violation and described corrective actions in a letter to the NRC dated May 3, 1991.

Due to an oversight, this item remained open in NRC records.

However, the

inspector was onsite at the time of the violation, recalls the licensee's immediate

corrective actions and actions to prevent recurrence,

and recalls that those actions

were appropriate

and effective.

The inspector confirmed that the licensee's

actions

were as described

in their May 3, 1991, letter, and concludes that no additional

action is warranted for this matter.

V. Mana ement Meetin

s

X1

Exit Meeting Summary

The inspectors presented

the inspection results to members of licensee management

at the

conclusion of the inspection on July 25, 1997.

In the meeting the licensee acknowledged

the findings presented.

The inspectors

asked the licensee whether any materials examined during the inspection

should be considered

proprietary.

No proprietary information was identified.

I

ATTACHMENT

PARTIAL LIST OF PERSONS CONTACTED

Licensee

W. E. Coley, Engineer,

Regulatory Services

W. G. Crockett, Manager, Nuclear Quality Services

T. F. Fetterman,

Director, Instrumentation

and Control Engineering

T. L. Grebel, Director, Regulatory Services

J. A. Gregerson,

Engineer, Engineer, Engineering Services

D. J. Hampshire, Senior Engineer,

Balance of Plant Engineering

M. J. Jacobson,

Manager, Nuclear Quality Services

S. C. Ketelsen, Senior Engineer, Regulatory Services

S. D. LaForce, Engineer Regulatory Services

J. E. Molden, Manager, Operations Services

M. G. Mosher,'Acting Director OSSP, Nuclear Quality Services

D. H. Oatley, Manager, Maintenance

Services

H, J. Phillips, Director, Engineering Services

R. P. Powers, Manager, Vice President

DCPP and Plant Manager

J. A. Shoulders,

Director, Support Engineering

R. L. Thierry, Engineer, Nuclear Technical Services

D. A. Vosburg, Director, NSSS Engineering Services

R. A. Waltos, Director, Engineering Services

R. C. Whitsell, Director, Nuclear Quality Services

INSPECTION PROCEDURES USED

IP 37551: Onsite Engineering

IP 61726: Surveillance Observations

IP 62707: Maintenance

Observations

IP 71707: Plant Operations

IP 71750: Plant Support

IP 92700: Onsite Followup of Written Reports of Nonroutine Events at Power Reactor

Facilities

IP 92902: Followup - Maintenance

IP 92903: Followup - Engineering

IP 92904: Followup - Plant Support

t

i

-2-

ITEMS OPENED, CLOSED, AND DISCUSSED

~Oened

50-275/97010-01

VIO

Failure to follow procedures

for alignment of 480V

power supply to instrument pan

I PY-16

50-275;323/97010-02

VIO

Failure to verify CIV SI-1(2}-8964 closed at least once

per 31 days

50-275/9701 0-03

NCV

Mode 3 entry with CCP inoperable due to total pump

flow exceeding

TS limit

50-275;323/9710-04

IFI

Unco trolled use of Dow Corning RTV-732 sealant in

containment

Closed

50-275/94023-00

LER

CCP flow greater than TS due to erosion of mini-flow

restricting orifice

50-275;323/9701 0-03

NCV

Mode 3 entry with CCP inoperable due to total pump

flow exceeding

TS limit

50-275/9506-02

IFI

'ASW vault drain calculation for medium energy line

break did not address

the limited capacity of the intake

structure sump pumps

50-275/96006-04

IFI

Licensee long-term corrective actions to improve source

range instrument reliability

50-275/9501 4-00

LER

Diesel Generators

started and loaded as designed

upon

failure of auxiliary transformer

1-1 due to

inadequate/Ineffective

procedures

relating to the control

of grounding devices

50-275;323/96021-06

URI

ASW TS interpretation more restrictive than TS

50-323/96023-05

50-275/9 'I 03-04

VIO

Failure to initiate an AR to address

loose fasteners

VIO

Inattentiveness

to Duties

Discussed

50-275;323/97-06-02

VIO

loose fasteners

on 4kV breaker cubicle

t

t

C

-3-

LIST OF ACRONYIVIS USED

AR

ASW

CCP

CCW

CFCU

CIV

DCPP

EDG

FSAR

IFI

LBIE

LER

MFP

NCV

NRR

OP

OTSC

PDR

RCS

SI

SR

TS

TVD

URI

1R8

action request

auxiliary saltwater

centrifugal charging pump

component cooling water

containment fan cooler unit

containment isolation valve

Diablo Canyon Power Plant

emergency diesel generator

final safety analysis report

inspection followup item

licensing basis impact evaluation

Licensee Event Report

main feedwater pumps

noncited violation

Office of Nuclear Reactor Regulation

Operations Procedure

on-the-spot-change

Public Document Room

reactor coolant system

safety injection

surveillance requirement

Technical Specification

test, vents, and drains

unresolved

item

Unit 1 eighth refueling

I

0-