ML16342A647

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Insp Repts 50-275/98-21 & 50-323/98-21 on 981204-18. Violations Noted.Major Areas Inspected:Operations & Maint. Generally Successful Response to Event Adversely Impacted by Several Performance Issues
ML16342A647
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 01/12/1999
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML16342A646 List:
References
50-275-98-21, 50-323-98-21, NUDOCS 9901200322
Download: ML16342A647 (32)


See also: IR 05000275/1998021

Text

ENCLOSURE 2

U.S. NUCLEAR REGULATORYCOMMISSION

REGION IV

Docket No

License No.:

Report No.:

Licensee:

Facility:

Location:

Dates:

Inspectors:

Contributing

Personnel:

Approved By:

50-275; 50-323

DPR-80; DPR-82

50-275/98-21; 50-323/98-21

Pacific Gas and Electric Company

Diablo Canyon Nuclear Power Plant, Unit 2

7 ~h miles NW of Avila Beach

Avila Beach, California

December 4 to 18, 1998

Scott A. Boynton, Senior Resident Inspector, WNP-2

Richard M. Pelton, Office of Nuclear Reactor Regulation

David L. Proulx, Senior Resident Inspector

Linda J. Smith, Acting Chief, Project Branch E

ATIACHMENTS:

Attachment

1

Attachment 2

Supplemental Information

Sequence

of Events

990i200322 990il2

PDR

ADQCK 05000275

8

PDR

e

EXECUTIVE SUMMARY

Diablo Canyon Nuclear Power Plant, Unit 2

NRC Inspection Report 50-275/98-21; 50-323/98-21

~Oerations

~

Overall, the operating crew responded satisfactorily to the degraded conditions in the

circulating water system and the manual reactor trip by effectively stabilizing the plant in

a safe condition. However, the generally successful response to the event was

adversely impacted by several performance issues (Section 04.1).

s

The crew did not understand the response of the intake screen differential pressure

indication to a unit trip, which led them to improperly leave Circulating Water Pump 2-2

operating and resulted in the screen differential pressure exceeding the design limits.

Weak fidelityamong the annunciator response procedures and an abnormal procedure

and the crew's narrow focus on pump motor amps also contributed to the delay in

securing the circulating water pump. One example of a violation of Technical Specification 6.8.1 was identified for failure to secure the pump in accordance with

abnormal operating procedures; however, because

the licensee implemented effective

corrective actions, no response was required (Section 04.1.b.4).

The crew's misunderstanding

of the effects of atmospheric dump valve pressure

setpoint adjustments on the reactor coolant system, coupled with a communication error

between the control operator and the shift foreman, resulted in a pressure setting of the

atmospheric dump valves that exceeded the setpoint specified in the procedure.

The

higher pressure setting unnecessarily challenged the main steam safety valves when it

contributed to the liftingof Main Steam Safety Valve RV-7. A second example of a

violation of Technical Specification 6.8.1 was identified for failure to implement

emergency operating procedure requirements; however, because the licensee

implemented effective corrective actions, no response was required (Section 04.1.b.5).

~

The management

process for collecting plant process information and evaluating

equipment response to the manual reactor trip was rigorous in identifying and

addressing equipment performance problems (Section 07.1).

~

~

The process for evaluating human performance lacked the same degree of formality

and structure as the management process for evaluating equipment response.

The lack

of structure, coupled with poor operating logs, made it difficultto reconstruct event

details and assess

the root cause of specific operator performance issues

(Section 07.1).

Maintenance

~

With the exceptions of the early liftof Main Steam Safety Valve RV-7 and the autostart

of Diesel Emergency Generator 2-2, plant equipment responded to the plant trip as

designed.

The licensee implemented appropriate corrective actions to address the low

setpoint on the main steam safety valve. The autostart of the diesel emergency

generator resulted from a long-standing design deficiency that had been previously

identified by the licensee and was not a safety concern.

The licensee had initiated

action to correct the deficiency prior to the plant trip (Section 02.1).

Re ort Details

Summa

of Plant Status

On December 4, 1998, Unit 1 operated at 50 percent power because

of a failed expansion joint

in the intake cooling system.

Operators returned Unit 1 to 100 percent power on December 5.

On December 17, operators shut down the reactor after identifying increased containment

sump leakage.

The licensee identified that the leak was from a weld on the component cooling

water supply line to Reactor Coolant Pump 1-3 upper bearing cooler.

Unit 1 was in Mode 3 at

the end of the inspection period.

Unit 2 was in Mode 3. Operators had manually tripped the reactor on December

1 because of

high kelp loading on the traveling screens.

Operators returned Unit 2 to full power on

December 9 following repairs to balance of plant equipment.

02

Operational Status of Facilities and Equipment

02.1

Plant E ui ment Performance

a.

Ins ection Sco

e 92901

The inspectors reviewed the sequence of events and compared it to the plant process

parameter data recorded during the event to determine the adequacy of plant

equipment performance.

Also, the inspectors evaluated corrective actions in which

equipment performance was not as expected.

b.

Observations and Findin s

In general, the plant responded as expected to the manual reactor trip, turbine trip, and

main steam isolation valve closure.

However, two safety-related components did not

respond to plant conditions as designed:

Main Steam Safety Valve RV-7 and Diesel

Emergency Generator 2-2. Main Steam Safety Valve RV-7 (nominal setpoint of

1065 psig) lifted unexpectedly when operators inappropriately raised steam generator

pressure to 1035 psig. The main steam safety valve lifted at a pressure just below its

Technical Specification pressure band of 1044 - 1097 psig. Subsequent

testing of the

main steam safety valve showed an as-found setpoint of 1039 psig, a pressure

consistent with the setting of the atmospheric dump valve pressure controllers. The

main steam safety valve was declared inoperable and its setpoint adju'sted within

1 percent of its Technical Specification-required value.

Valve RV-7 was the low

setpoint safety valve on Main Steam Lead 2.

To evaluate the generic implications of the low liftpoint on Main Steam Safety

Valve RV-7, the licensee tested Main Steam Safety Valves RV-3 and RV-8 on Steam

Leads

1 and 2, respectively.

The as-found pressure setpoints for both valves were

found to be within Technical Specification limits and the licensee concluded it was not

necessary to test other valves. The licensee selected these main steam safety valves

because

the valves had low values for their pressure setpoint and had been refurbished

at the same time as Main Steam Safety Valve RV-7. The inspectors determined that

corrective actions associated

with Main Steam Safety Valve RV-7 were appropriate.

-2-

Following the reactor trip, the electrical supply to the 4160V vital busses transferred to

the startup transformer.

Although the transfer to startup power is designed to preclude

a start of the diesel emergency generators,

Diesel Emergency Generator 2-2

autostarted; however, Diesel Emergency Generator 2-2 did not load onto its associated

vital bus, Bus H. This phenomenon,

which had occurred on two previous plant trips,

was previously evaluated by the licensee and determined to result from relatively light

electrical loading on Bus H. This light bus loading translated to a slow voltage decay

when the auxiliary feeder breaker opens.

The slow voltage decay allows the first level

undervoltage relay to time-out and start Diesel Emergency Generator 2-2 prior to

reaching the low voltage setpoint that closes the startup feeder breaker to Bus H. The

phenomenon

had also been observed, in one instance, with Diesel Emergency

Generator

1-1 on Unit 1.

To determine the impact of the inadvertent starts of Diesel Emergency Generators

1-1

and 2-2, the inspectors compared the number of inadvertent starts to the total number of

start demands placed upon the two diesel emergency generators.

Since 1992, there

had been oyer 500 start demands placed on Diesel Emergency Generators

1-1 and 2-2.

Of those starts, four resulted from a slow voltage decay on the vital bus following a unit

'rip. Therefore, the inspectors concluded that the inadvertent starts did not significantly

impact component aging or reliability of the diesel emergency generators.

To correct the deficiency, the licensee submitted a license amendment request in

October 1998 to set the first level undervoltage relays to a lower value. The lower value

is expected to limitthe time between the start of the first level undervoltage relay timer

and the low voltage setpoint that closes the startup feeder breaker.

Thus, the timer

would not time-out prior to restoring bus voltage from startup power.

Conclusions

With the exceptions of the early liftof Main Steam Safety Valve RV-7 and the autostart

of the Diesel Emergency Generator 2-2, plant equipment responded to the plant trip as

designed.

The licensee implemented appropriate corrective actions to address the low

setpoint on the main steam safety valve. The autostart of the diesel emergency,

generator resulted from a long-standing design deficiency that was not a safety concern.

The licensee had initiated action to correct the deficiency prior to the plant trip.

Operator Knowledge and Performance

0 erator Res

onse to Loss of Main Condenser and Manual Reactor Tri

Ins ection Sco

e 92901

The inspectors evaluated operator performance in preparing for and responding to the

degraded intake conditions and manual reactor trip. Specifically, the inspectors

evaluated command and control, operator knowledge, internal and external

communications, and procedure use and adequacy.

0

-3-

In responding to the plant conditions produced by'the high sea state, operators utilized

the following procedures:

ARP PK13-04, "Condenser Delta P Hl PPC," Revision 3

OP AP-7, "Degraded Condenser," Revision 17

OP L-7, "Plant Stabilization Following Reactor Trip," Revision 2

OP 0-28, "Intake Management," Revision 2

EOP E-O, "Reactor Trip or Safety Injection," Revision 12

EOP E-0.1, "Reactor Trip Response," Revision 13

Observations and Findin s

b.1

Communications

Attachment

1 to Procedure OP1.DC11, "Conduct of Operations - Abnormal Plant

Conditions," Revision 12, stated that three-way communications were the standard for

communication.

This standard was established during the 1998 training cycle and had

been in place for approximately 6 months.

From operator interviews, the inspectors

determined that three-way communications were not consistently utilized during the

event and tended to degrade as the event progressed.

The inspectors validated this

finding through direct observation of two separate crews on the plant simulator and

control room observations of the Unit 2 plant startup.

In each observation, inconsistent

use of three-way communication indicated that three-way communication had not yet

become a habit with the operators.

The lack of complete three-way communications

only resulted in one identified human performance error. Specifically, inadequate three-

way communications between the control operator and the shift foreman contributed to

the improper setting of the 10 percent atmospheric dump valve controllers discussed

below in Section 04.1.b.5.

Prior to the manual reactor trip, the operating crew was cognizant of the degrading

conditions in the Unit 2 main condenser and established a conservative'action

level to

reduce plant load when condenser quadrant differential pressure reached 9 psid (plant

procedures require load reduction at 10 psid). Subsequently, condenser quadrant

differential pressure continued to increase at a rate of between 0.5 and 1.0 psid/hr.

Procedure OP 0-28, "Intake Management," Revision 2, recommended

notification of the

operations services manager and the operations director if it was likelythat a load

decrease

will be required.

However, operations management was not notified of the

potential need to reduce plant load. Early notification of operations management would

have allowed management

to be involved in the decision process regarding continued

plant operations.

b.2

Command and Control

Overall, the shift foreman demonstrated

good performance in carrying out his control

room command responsibilities.

Assignment of the senior control operator to monitor

circulating water and condenser conditions ensured timely closure of the main steam

isolation valves when Circulating Water Pump 2-2 was secured.

Proper focus of the

-4-

balance-of-plant control operator on auxiliary feedwater allowed for timely identification

of the feedf low mismatch on Steam Generator 2-2 and investigation of a possible steam

or feedwater leak.

One weakness was identified in regard to crew briefings. Crew briefings were not

performed when the operators transitioned to Procedure EOP E-0.1, "Reactor Trip

Response,"

Revision 13, or when they transitioned to Procedure OP L-7, "Plant

Stabilization Following Reactor Trip," Revision 2. The lack of briefings was inconsistent

with management expectations as specified in Procedure OP1.DC11.

The briefings

would have been beneficial in: (1) highlighting the overall strategy of the procedures,

(2) emphasizing specific actions and the threshotds at which they are taken, and

(3) assigning specific crew responsibilities for those actions, as necessary.

Detailed

briefings were also not conducted prior to use of Procedures

OP 0-28 and OP AP-7,

"Degraded Condenser," Revision 17. These procedures addressed

the potential

consequences

of the high swell warning in effect and provided specific strategies for

protecting the normal plant heat sink. Discussing the strategies could have highlighted

the requirement to immediately secure a circulating water pump when the intake screen

differential pressure exceeded the design limitof 50 iwg specified in Procedure 0-28,

Section 6.3.

The shift foreman also failed to ensure that actions were completed to reset the

atmospheric dump valve pressure controllers in accordance with Procedure EOP E-0.1,

as discussed below in Section 04.1.b.5.

b.3

Procedure Use and Ade uac

Prior to the reactor trip, operators responded to several alarms associated with main

condenser and intake screen differential pressures.

No information was found to

indicate that the annunciator response procedures associated

with the alarms were not

properly implemented.

However, the inspectors noted a gap between

Procedures ARP PK13-04 and OP AP-7 that did not provide for a smooth transition

between the two procedures and contributed to a delay in taking actions.

The entry

criteria for Procedure ARP PK13-04 were lower than the action criteria in

Procedure OP AP-7. Specifically, Procedure ARP PK13-04 was entered when an alarm

was received for one or more of the following conditions:

~

Condenser quadrant differential pressure at 9.5 psid

~

Condenser quadrant differential pressure at 12.5 psid

~

Rate-of-change

in differential pressure is greater than 0.5 psid/hr when quadrant

differential pressure

is greater than 7.0 psid in any quadrant.

If any of the above conditions was determined to be valid, then operators were directed

to implement Procedure OP AP-7. However, Procedure OP AP-7 did not require any

actions to be taken until condenser quadrant differential pressure exceeded

10.0 psid.

With differential pressures

below this criterion, Procedure OP AP-7 directs operators to

return to the procedure and step in effect (e.g., Procedure ARP PK13-04). Thus, prior

0

-5-

to the plant trip at 3:47 a.m. with condenser quadrant differential pressures less than

10.0 psid,.the operating crew did not believe they had formally entered

Procedure OP AP-7. This contributed to the crew briefing weakness discussed above in

Section 04.1.b.2.

At 3:45 a.m., when Circulating Water Pump 2-2 intake screen differential pressure

exceeded

100 iwg, operators promptly initiated a rapid downpower of the unit to prepare

to remove the circulating water pump from service.

Within approximately

1 minute, with

screen differential pressure remaining greater than 100 iwg, the shift supervisor

recommended and the shift foreman directed a manual reactor trip. Although not

required by procedure, operators initiated the manual reactor trip based upon already

degraded conditions in the main condenser.

The inspectors concluded that the decision

by the shift supervisor and shift foreman was appropriate and demonstrated a good

awareness

of plant conditions.

b.4

Circulatin

Water Pum

2-2 Tri

Although the manual reactor trip was initiated based upon the threat of damage to

Circulating Water Pump 2-2 and loss of the normal heat sink, operators did not secure

the circulating water pump.

Both Procedures

OP 0-28 and OP AP-7 provided direction

to immediately secure the circulating water pump under the high differential pressure

conditions observed.

Procedure OP 0-28 stated that "ifscreen differential pressure

increases to the point where failure is imminent, or if the screens stop running, the

[circulating water pump] must be immediately secured, even if this requires a reactor

trip." Procedure OP AP-7 specifically requires the circulating water pump to be secured

when screen differential pressure exceeds 50 iwg, the design differential pressure for

screen integrity.

Following the reactor trip and entry into Procedure EOP E-O, the senior control operator

continued to focus on the condition of Circulating Water Pump 2-2 by monitoring the

pump motor amps to look for indication of pump cavitation.

In addition, the transfer of

electrical power to the startup transformer resulted in the temporary loss of the Unit 2

intake screen differential pressure signal and an erroneous indication of 0 iwg across

the intake screens for Circulating Water Pump 2-2. The senior control operator,

believed the indication was valid and took no action to secure the pump.

Although valid indication of the intake screen differential pressure was restored in

approximately 2 minutes, the continuing high differential pressure was not recognized

for another 4 minutes when pump motor amps began to fluctuate from pump cavitation.

Thus, the failure to secure the circulating water pump before damage occurred to the

intake screens resulted from both a lack of understanding of the response of the screen

differential pressure indication following a Unit 2 trip and a narrow focus on pump motor

'mps.

The licensee indicated they would implement a method to ensure the screen

differential pressure indications are more reliable.

In addition, the licensee willdiscuss

this error in licensed operator training.

0

-6-

The failure to immediately secure Circulating Water Pump 2-2 when its associated

screen pressure exceeded 50 iwg was identified as one example of a violation of

Technical Specification 6.8.1 for failure to implement the procedural requirements of

Procedure OP AP-7 (50-323/98021-01).

b.5

Im ro er Pressure Settin

for Atmos heric Dum

Valves

When implementing the requirements of the "response not obtained" column in

Procedure EOP E-0.1, Step 10.d, because of the unavailability of the main condenser,

the control operator began lowering the pressure setpoint of the atmospheric dump

valves to 1005 psig. However, when the atmospheric dump valves began to open in

response to lowering the setpoint, the operator mistakenly believed that the valve

response would result in an excessive cooldown of the reactor coolant system and

improperly returned the setpoints to 1035 psig. As noted above, an apparent

'

miscommunication between the control operator and shift foreman also contributed to

the improper setting.

Shortly thereafter, Steam Generator 2-2 Main Steam Safety

Valve RV-7 lifted because of the proximity of its liftsetpoint to steam generator

pressure.

Personnel statements and operator interviews indicated that, following the resetting of

the atmospheric dump valve pressure controllers to 1035 psig; the intent was to slowly

lower the pressure setpoints to 1005 psig. However,.plant computer data showed that

the setpoints were not adjusted until 8 a.m. when pressure was lowered to

approximately 980 psig to successfully reseat Main Steam Safety Valve RV-7. Both

Procedures EOP E-0.1 and OP L-7 directed that operators reset the pressure controllers

for the atmospheric dump valves from a setpoint of 1035 psig to a setpoint of 1005 psig

when the main condenser is unavailable.

This action would allow the atmospheric dump

valves to stabilize reactor coolant system temperature at the no-load average

temperature of 547'F.

It also prevents interaction between the atmospheric dump

valves and the low setpoint main steam safety valves that are set at 1065 psig.

In an incident summary developed by the operations director, the performance issues

that resulted in the improper setting of the atmospheric dump valve pressure controllers

were identified and corrective actions were developed.

Specifically, the licensee

corrective actions included:

(1) having procedure writers ensure that the wording is

properly human factored, and (2) describing the error as part of the trip response

discussion in industry events training. The failure to set the pressure controllers for the

atmospheric dump valves in accordance with Procedure EOP E-0.1 is a second

example of a violation of Technical Specification 6.8.1 for failure to followprocedures

(50-323/98021-01).

b.6

0 erator Knowled e

Two operator knowledge deficiencies were identified that adversely impacted the event

response.

In evaluating the condition of Circulating Water Pump 2-2 and its associated

intake screens,

the crew was unaware that, upon a Unit 2 trip, indication of intake

e

-7-

screen differential pressure is temporarily lost and willindicate as 0 iwg until the signal is

restored.

Believing the indication of 0 iwg was valid following the manual reactor trip,

the crew delayed securing the circulating water pump.

In stabilizing the plant in accordance with Procedure EOP E-0.1, the control operator

misunderstood the response of the plant to adjustments of the pressure controllers of

the atmospheric dump valves. The control operator, believing that adjustment of the

pressure controllers to 1005 psig could result in an excessive cooldown, reset the

controllers back to 1035 psig, contrary to procedural requirements.

However, an

adjustment of 30 psig on the pressure controllers equates to less than a 5 F change in

reactor coolant system temperature.

Conclusions

Overall, the operating crew responded satisfactorily to the degraded conditions in the

circulating water system and the manual reactor trip effectively stabilized the plant in a

safe condition. However, the generally successful response to the event was adversely

impacted by several performance issues.

The crew's misunderstanding

of the effects of atmospheric dump valve pressure

setpoint adjustments on the reactor coolant system, coupled with a communication error

between the control operator and the shift foreman, resulted in a pressure setting of the

valves that exceeded the setpoint specified in the procedure.

The higher pressure

setting unnecessarily challenged the main steam safety valves when it contributed to the

lifting of Main Steam Safety Valve RV-7. One example of a violation of Technical Specification 6.8.1 was identified for failure to implement emergency operating

procedure requirements; however, because

the licensee planned effective corrective

actions, no response was required.

The crew did not understand the response of the intake screen differential pressure

indication to a unit trip, which led them to improperly leave Circulating Water Pump 2-2

operating and resulted in screen differential pressure exceeding the design limits. Weak

fidelityamong the annunciator response procedures and an abnormal procedure and

the crew's narrow focus on pump motor amps also contributed to the delay in securing

the circulating water pump. A second example of a violation of Technical Specification 6.8.1 was identified for failure to secure the pump in accordance with

abnormal operating procedures; however, because the licensee planned effective

corrective actions, no response was required.

0

-8-

07

Quality Assurance in Operations

07.1

Licensee Event Reconstruction and Assessment

Ins ection Sco

e 92901

The inspectors reviewed documentation available to support event reconstruction and

assessment.

Based upon the available information, an evaluation was made of the

depth and scope of the self-critique.

Observations and Findin s

The self-assessment

of the event was generally thorough; however, it was hampered by

poor documentation.

The operating logs of the shift foreman, the control operator, and

the turbine building watch were inadequate to reconstruct the significant activities

associated with the event response.

Neither the shift foreman nor the control operator

logs document the closure of the main steam isolation valves, indications of the liftingof

Main Steam Safety Valve RV-7, or the entry into Procedure OP L-7. Between 3:47.a.m.

and 6 a.m., a period when actions were being taken in accordance with

Procedures OP AP-7, EOP E-O, EOP E-0.1, and OP L-7, no entries were made in the

shift foreman's log. The level of detail in the operating logs was not consistent with the

recommendations

in Procedure OP1.DC37, "Plant Logs," Revision 12.

Although a postshift critique with the'operators involved in the trip response

is

recommended

by Procedure OP1.DC1, "Administrative Program to Control the Return

to Power After a Reactor Trip," Revision 2A, the licensee did not complete the review

after shift change immediately following the event. The use of a group debriefing is also

recommended by Procedure XI1.ID3, "Event Investigation Team, Event Response

Team, and Event Investigation Report," Revision 0. The licensee determined that this

was a missed opportunity to collect information details that are forgotten over time and

to identify the improper setting of the atmospheric dump valves, which was first

identified by the NRC resident inspectors.

The licensee determined that they would

have eventually identified the improper setting of the atmospheric dump valves during

their posttrip review.

Procedure XI1.ID3 required written statements to be obtained from each person

involved in the event that describe their observations and actions regarding the

circumstances of the event.

It further states that the statements should be obtained as

soon as practical after the event and prior to the involved individuals leaving site.

However, personnel statements

regarding the event did not meet this recommendation.

Only three statements were obtained immediately after the event, while the last

statement, from the shift technical advisor, was not obtained until 3 days later.

Further,

the information provided in the personnel statements

did not provide sufficient detail to

fill in the gaps in the operating logs. This included information regarding entry into and

exit from Procedure OP AP-7, time of exit from the emergency operating procedures,

and the basis for not returning the pressure control setpoint of the atmospheric dump

valves to 1005 psig after reseating Main Steam Safety Valve RV-7.

-9-

To help fillin the information gaps in the control room logs and personnel statements,

the operations director met with the operating crew involved with the trip response

2 days after the event to develop an incident summary and lessons learned.

The

incident summary effectively captured the significant performance issues.

C.

In reviewing the requirements and guidance in Procedure OP1.DC1, the inspectors

concluded that the procedure provided adequate

requirements for collection and

archiving of information related to equipment and plant performance concerns.

However, the requirements for collecting information and assessing

human performance

were not as clear. As stated above, it was only recommended to conduct a postshift

critique with the involved crew. Additionally, the procedure did not give specific

guidance to operators regarding the appropriate level of detail needed in their personnel

statements.

Attachment 6.1 of Procedure OP1.DC1 did not require an assessment

of

human performance.

I

Conclusions

The management

process for collecting plant process information and evaluating

equipment response to the manual reactor trip was rigorous in identifying and

addressing equipment performance problems.

The process for evaluating human

performance lacked the same degree of formality and structure.

The lack of structure,

coupled with poor operating logs, made it difficultto reconstruct event details and

assess

the root cause of specific operator performance issues.

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management

at the

conclusion of the inspection on December 18, 1998. The licensee acknowledged the findings

presented.

The inspectors asked the licensee whether any materials examined during the inspection

should be considered proprietary.

No proprietary information was identified.

Attachment

1

Supplemental Information

PARTIALLIST OF PERSONS CONTACTED

Licensee

J. Molden, Operations Services Manager

W. Garrett, Operations Director

B; Lewis, Senior Operations Supervisor

J. Haines, Operations Training

G. Goelzer, Shift Supervisor

M. Wright, Shift Foreman

W. Bumen, Senior Control Operator

R. Kline, Control Operator

A. Duracher, Balance of Plant Control Operator

IP 92901:

INSPECTION PROCEDURES USED

Followup - Operations

ITEMS OPENED, CLOSED, AND DISCUSSED

0 ened and Closed

50-323/98021-01

VIO

failure to secure circulating water pump in accordance with

abnormal procedures and failure to properly set atmospheric

dump valve pressure controllers in accordance with emergency

operating procedures (Sections 04.1.b.4 and 04.1.b.5)

0

Attachment 2

SEQUENCE OF EVENTS

(Alltimes are noted in PST)

Date/Time

11/30/98

8:00 p.m.

12/1/98

- 12:00 a.m.

12/1/98

- 2:00 a.m.

12/1/98

- 3:00 a.m.

12/1/98

3:15 a.m.-

3:30 a.m.

12/1/98

3:45 a.m.

Event

High swell warning in effect. Circulating water differential pressure across

the Unit 2 condenser approximately'5 psid. A senior control operator is

stationed at the intake structure in accordance with Procedure OP 0-28,

"Intake Management."

Because of rising differential pressure across the Unit 2 condenser (6 psid),

the shift supervisor and Unit 2 shift foreman agree to curtail the unit to

50 percent power if differential pressure reaches

9 psid.

Note: Procedure OP AP-7, "Degraded Condenser," directs curtailment when

condenser differential pressure exceeds

10 psid.

Differential pressure across the Unit 2 condenser increased to approximately

7 psld.

Maximum condenser limiting differential pressure is greater than 8 psid and

rising at approximately 2 psid/hr. Large bed of kelp observed floating in front

of the Unit 2 intake screens.

Based upon conditions in the condenser,

Procedure AR PK13-04, "Condenser Delta P Hi PPC," directs entry into

Procedure OP AP-7. No actions currently required by the abnormal

procedure.

Several manual and automatic actions were taken to vary intake screen

speed in response to high screen differential pressure and a continuing rise

on condenser differential pressure.

Unit 2 condenser limiting differential

pressure approaching 9 psid.

Rapid rise observed on the differential pressure across the circulating water

Pump 2-2 intake screens to greater than 100 iwg. The Unit 2 shift foreman

directs a rapid power decrease

at a ramp rate of 50 percent.

12/1/98

3:47 a.m.

NOTE: Procedure OP AP-7 required the affected circulating water pump to

be tripped when its associated

intake screen differential pressure is greater

than 50 iwg.

Based upon the high differential pressure across the Circulating Water

Pump 2-2 intake screen, the shift foreman directs the control operator to trip

the reactor.

The reactor trip was not required by procedure.

0

-2-

Date/Time

12/1/98

3:47 a.m.+

Event

Circulating Water Pump 2-1 trips as expected upon transfer of Unit 2

electrical loads to startup power. Light electrical loading on vital 4160V vital

Bus H results in a relatively slow bus voltage decay and a start of Diesel

Emergency Generator 2-2.

12/1/98

3:49 a.m.

12/1/98

3:53 a.m.

Operators leave Circulating Water Pump 2-2 operating based upon an

erroneous pressure indication of 0 iwg. The 0 iwg pressure reading from the

plant process computer is actually the result of a temporary loss of power to

its associated signal processor during the transfer to startup power.

Unit 2 intake screen differential pressure signal is restored in the control room

and reads greater than 100 iwg. However, this is not observed by control

room operators.

Senior control operator observes Circulating Water Pump Motor 2-2 current

swings of approximately 20-30 amps and secures the pump. This action is

consistent with Procedure OP AP-7.

12/1/98

3:54 a.m.

12/1/98

4:10 a.m.

12/1/98

- 4:12 a.m.

12/1/98

4:17 a.m.

12/1/98

- 4:45 a.m.

12/1/98

':55

a.m.

12/1/98

- 5:30 a.m.

With loss of all circulating water, the senior control operator recommends and

the shift foreman directs the closure of the main steam isolation valves.

Procedure EOP E0.1, "Reactor Trip Response,"

is entered.

Source:

control

operator log.

Control operator adjusts atmospheric dump valve pressure control setpoints

from 1035 psig to 1005 psig in accordance with Procedure EOP E0.1.

Because of a miscommunication with the shift foreman, the control operator

readjusts the atmospheric dump valve pressure control setpoints back to

1035 psig.

Steam Generator 2-2 pressure increases to approximately 1040 psig and

Main Steam Safety Valve RV-7 opens.

Steam Generator 2-2 pressure falls to

approximately 1005 psig and stabilizes with the relief valve remaining partially

open.

This valve has a nominal setpoint of 1065 psig.

Procedure OP L-7, "Plant Stabilization Following a Reactor Trip," is entered.

Vacuum broken on the Unit 2 main condenser.

This action is directed by

Procedure EOP E0.1.

Source: plant process computer

Operators observe a low water level condition in Steam Generator 2-2 and a

higher than expected auxiliary feedwater flow. Actions are initiated to restore

water level in Steam Generator 2-2 and operators are dispatched to

investigate a possible steam leak. Source:

PSRC meeting minutes

0

e

-3-

Date/Time

12/1/98

- 6:30 a.m.

Event

Observations at the Steam Lead 2 pipe rack area identify that Main Steam

Safety Valve RV-7 is open.

12/1/98

8:19 a.m.

Shift turnover to the oncoming operating crew is in progress and the shift

supervisor and shift foreman make a conscious decision to delay actions to

reseat the main steam safety valve until completion of turnover. This

decision was based upon the stability of reactor plant parameters and the

desire to carefully plan those actions.

Lowering of the Steam Generator 2-2 atmospheric dump valve pressure

control setpoint successfully reseats Main Steam Safety Valve RV-7 at a

pressure of 987 psig.