ML16342E077

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Insp Repts 50-275/98-07 & 50-323/98-07 on 980215-0328. Violations Noted.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support
ML16342E077
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 04/22/1998
From: Wong H
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML16342E075 List:
References
50-275-98-07, 50-275-98-7, 50-323-98-07, 50-323-98-7, NUDOCS 9804280121
Download: ML16342E077 (70)


See also: IR 05000275/1998007

Text

ENCLOSURE 2

U.S. NUCLEAR REGULATORYCOMMISSION

REGION IV .

Docket Nos.:

50-275

50-323

License Nos.:

DPR-80

DPR-82

Report No.:

Licensee:

Facility:

Location:

Dates:

Inspector(s):

50-275/98-07

50-323/98-07

Pacific Gas and Electric Company

Diablo Canyon Nuclear Power Plant, Units 1 and 2

7 '/~ miles NW of Avila Beach

Avila Beach, California

February 15 through March 28, 1998

D. L. Proulx, Senior Resident Inspector

D. B. Allen, Resident Inspector

D. G. Acker, Project Inspector

T. R. Meadows, Licensing Examiner

W. M. McNeill, Reactor Inspector

B. J. Olson, Project Inspector

Approved By:

H. J. Wong, Chief, Reactor Projects Branch E

Attachment:

Supplemental Information

9804280121

980422

PDR

ADQCK 05000275

PDR

-2-

EXECUTIVE

UMMARY

Diablo Canyon Nuclear Power Plant, Units 1 and 2

NRC Inspection Report 50-275/98-07; 50-323/98-07

This inspection included aspects of licensee operations, maintenance,

engineering, and plant

support.

The report covers a 6-week period of resident inspection.

~Oera ions

Shutdown and startup evolutions were conducted in a professional manner, in

accordance with procedures and a focus on safety (Section 01.1).

A noncited violation, per Section VII.B.Iof the NRC Enforcement Policy, was identified

for failure to provide a procedure appropriate to the circumstances for switching of

power supplies between the units. The switching of the power supply without clearly

understanding the outcome resulted in unexpected alarms, loss of power to equipment

required by Technical Specifications, and unnecessary

disruption in both control rooms.

The immediate response of the Unit 1 control room operators was very good, with timely

and appropriate response to each alarm (Section 01.2).

A violation was identified for failure to provide a midloop procedure appropriate to the

circumstances that required proper stowage of a nonseismically qualified hoist. The

hoist was left in an unstowed condition above the operating residual heat removal pump

during a reduced inventory condition (Section 01.3).

Several significant operator evolutions were performed well. Shutdown and startup

evolutions were conducted well, in a professional manner, in accordance with

procedures,

and with a focus on safety.

Licensee preparations and implementation,

including the operations pre-evolution briefings for early midloop operations, were

conservative and reflected a focus on safety.

The reflood of the emergency core cooling

systems evolution was well coordinated and controlled, with each participant aware of

their responsibilities. The pre-evolution briefing w'as comprehensive,

with emphasis on

safe, cautious performance and the necessity for good communications

(Sections 01.3 and 01.4).

A violation was identified for failure to restore the "High Flux at Shutdown" annunciator

when the required number of fuel assemblies was installed in the core. The

responsibility to perform the actions was not clearly assigned prior to the evolution

(Section 01.5).

The control of refueling activities lacked clear procedural guidance and management

expectations.

The lack of procedural guidance for performing signal-to-noise ratio

calculation, the lack of acceptance

criteria in the procedure for fuel assembly

clearances,

and the confusing procedure format were weaknesses

in the procedure.

The method used to calculate inverse count rate ratio and the method used to perform

-3-

the post core load verification were inconsistent with the methods described in the

procedure.

The lack of separate signatures in the controlled copy of the procedure for

verifying that the signal-to-noise ratio was greater than two was an example of poor

documentation of procedurally required activities (Section 01.5).

Aviolation was identified for several examples of failure to properly implement the

clearance procedure.

However, the number and significance of clearance errors in

Refueling Outage 2R8 were improved from the previous outage.

Several significant

errors were not found or prevented by the clearance process and resulted in the

potential for work to be performed without the required isolation from sources of energy

to allow safe work (Section 01.6).

A violation was identified for failure to translate the design of the reactor vessel refueling

level indication system into abnormal operating procedures.

The licensee exhibited

good attention to detail in identifying this issue during simulator training. Documented

corrective actions at the end of the inspection period for this violation failed to address

deficiencies in the procedure preparation and approval process (Section 03.1).

The training provided for Unit 2 outage preparation was implemented well and provided

valuable lessons learned and necessary

procedural changes.

The inspectors noted, in

particular, that the simulator training was professional, well executed, and identified a

vulnerability in the abnormal operating procedures (Section 05.1).

aine

ance

Maintenance personnel did not exercise appropriate care during penetration seal work

and stepped on a valve, that when repositioned, challenged operators by causing a leak

in the chemical and volume control system (Section 02.1).

A number of maintenance activities were observed and were performed in accordance

with the procedural requirements.

Good coordination between technical maintenance,

mechanical maintenance,

and radiation protection was obser ved in performing several

maintenance tasks concurrently on the containment spray pump, thereby reducing the

time the pump was inoperable due to maintenance (Section M1.1).

The inspectors observed a number of surveillance tests and found that the surveillances

observed were performed in a cautious manner with self-checking and proper

communications employed.

The procedures governing the surveillance tests were

technically adequate

and personnel performing the surveillances demonstrated

an

adequate

level of knowledge.

The inspectors noted that test results appeared to have

been appropriately dispositioned (Section M1.2).

The containment cleanup and closeout activities were appropriately controlled, and the

material condition of containment areas was satisfactory for restart. of Unit 2

(Section M1.3).

The license's approach to the inspection of part length control rod drive mechanism

welds was sound and aggressive. The inspectors found the ultrasonic testing showed

the seven motor tubes'pper and lower transition welds were free of the type of defect

found at Prairie Island on the G-9 motor tube (Section M2.1).

'

A noncited violation was identified for failure to provide a procedure appropriate to the

circumstances for ground buggy installation. The improper ground buggy installation

had the potential to have caused significant damage to safety-related equipment and

injure workers (Section M4.1).

The inspectors concluded that the corrective actions for Violation 50-275;323/96014-03

were sufficiently directed towards ensuring that control board action request stickers

were removed when the work was complete, but did not appear to fullyaddress the

need to closely control these deficiency tags. The inspectors found six additional

deficiencies concerning control board action requests.

Therefore, the licensee's

programs to ensure that the control board action requests stickers reflected the

licensee's tracking list and the up-to-date plant configuration warranted further licensee

attention (Section M8.1).

~En ineerin

The inspectors concluded that the design change package and associated safety

evaluation for replacement of the Unit 2 recirculation sump screens was comprehensive,

and the conclusions were reasonable.

The design change was effective in improving

the containment sump's ability to screen out debris that could block safety injection flow

paths (Section E2.1).

Plan Su

ort

~

Licensee management's

efforts to keep exposures as low as reasonably achievable

during Refueling Outage 2R8 appeared to be successful in that total outage exposure

was improved from previous outages.

The licensee's cleanup of the reactor coolant

system following shutdown of Unit 2, and the use of mock-up training for several outage

tasks contributed to the lower exposure (Section R1.1).

Re ort Details

Sum

a

of Plan

S a us

Unit 1 began this inspection period at 100 percent power.

On March 21 1998, reactor power,

was reduced to 50 percent to conduct main feedwater pump control and stop valve testing, and

Unit 1 was returned to 100 percent power later that day.

Unit 1 continued to operate at

essentially 100 percent power until the end of this inspection period.

Unit 2 began this inspection period in Mode 4 (Hot Shutdown) for Refueling Outage 2R8.

On

March 24, on completion of outage activities as of that point, Unit 2 entered Mode 2 (Startup).

On March 25, Unit 2 entered Mode 1 (Power Operation).

Later on March 25, the turbine tripped

prior to synchronizing to the grid, and Unit 2 was returned to Mode 3 (Hot Standby) to

investigate a turbine lube oil system problem.

After completing repairs in the lube oil system,

the reactor was returned to Mode 2 on March 27 and entered Mode 1 later that day. On

March 28, Unit 2 was synchronized to the grid, ending Refueling Outage 2R8. Unit 2 was at

30 percent power at the end of this inspection period.

i. ~0erations

01

Conduct of Operations

01.1

General Commen s

1707

The inspectors observed control room operations and toured the plant on a frequent

basis, including frequent backshift inspections.

In general, the performance of plant

operators was professional and reflected a focus on safety.

Operators continued to

perform well, utilizing three way communications and self-checking techniques.

Operator response to alarms were observed to be prompt and appropriate to the

circumstarices.

Operations shift management were frequently present in the control

room and were aware of plant conditions. All crew members interviewed by the

inspectors were aware of plant conditions and system configurations.

Limiting

conditions for operations were properly entered when required.

During this period the

inspectors observed several crews for each unit, including backshifts.

The inspectors

noted increase operations department management presence

in the control room during

the Unit 2 shutdown.

The inspectors observed portions of reactor startup activities

between March 25-March 28. The inspectors noted that these startup activities were

conducted in a professional manner, in acc'ordance with procedures,

and with a focus

on safety.

01.2

Transferrin

Power Su

I

For Ins rument Dis ribution Panel PYNM

a.

Ins ection Sco

e 71707

On February 10, the inspectors observed control room activities while systems and

equipment with unit cross-ties were being realigned to Unit 1 prior to the Unit 2 refueling

outage (2R8).

-2-

Observa io s and Findi

s

While transferring the power supply for Panel PYNM (a 208/120 volt instrument

distribution panel) from Unit 2 to Unit 1, a number of unexpected alarms were received

in both Unit 1 and Unit 2 control rooms. The operator performing the switching had not

expected the alarms and had informed the Unit 2 shift foreman that there would be no

alarms in the control room during the switching. The drawing the operator had

referenced did not have sufficient information to identify the effects of the transfer.

Had

the correct drawings been used, each alarm would have been anticipated or actions

taken to prevent the alarms from occurring. Action Request A0452798 was initiated to

document this occurrence

The alarms received included: fire detection, component cooling surge tank pressure

high and low, seismic trip undervoltage, post accident sample room radiation monitor

failure, and low flow to Radiation Monitors RM-11 and RM-12. The seismic trip system

provided an input to reactor trip at Diablo Canyon.

Radiation Monitor RM-11 was the

containment air particulate monitor and RM-12 was the containment radioactive gas

monitor. Technical Specification 3.4.6.1, "Reactor Coolant System Leakage Detection

Systems" requires that with both Radiation Monitors RM-11 and RM-12 inoperable, the

containment fan cooler collection monitoring system and the containment structure

sumps and reactor cavity sump level and flow monitoring systems must be operable.

The inspector observed the Unit 1 control room operators respond to these alarms.

The

control operator immediately evaluated and prioritized the alarms by importance. The

Unit 1 shift foreman questioned the Unit 2 shift foreman and learned that the alarms

could have been caused by the switching of power to Panel PYNM, and relayed this

information to the control operator.

Follow up actions to return equipment and alarms to

normal was appropriate and timely. Both units entered Technical Specifications action

statements for loss of Radiation Monitors RM-11 and RM-12.

The switching of power was performed under the direction of an Operations Section

Policy DP, "Preoutage System Alignments For Systems With Unit Crossties,"

Revision 1. There was not a procedure available to perform this switching. For six

other activities addressed

by the policy, specific procedures were referenced to perform

the transfer.

The policy document was not a procedure and provided no guidance as to

the expected results.

The procedures referenced

in the policy did not provide the

necessary directions.

As corrective actions, the licensee committed to revise Operations Section Policy D-4

and the applicable procedures referenced in the policy such that clear procedural

guidance would be provided for future power switching operations.

In addition, the

licensee placed a permanent operator aide near Panel PYNM to alert the operators of

the multiple inputs to the panel.

Failure to provide a procedure appropriate to the circumstances for switching power

supplies is a violation of 10 CFR Part 50, Appendix B, Criterion V. However, this

-3-

nonwillful, self-revealing, and corrected violation is being treated as a noncited violation,

consistent with Section VII.B.1 of the NRC Enforcement Policy (50-275;323/98007-01).

c.

Conclusions

A noncited violation was identified for failure to provide a procedure appropriate to the

circumstances for switching of power supplies between the units. The switching of the

power supply without clearly understanding the outcome resulted in unexpected alarms,

loss of power to equipment required by Technical Specifications, and unnecessary

disruption in both control rooms. The immediate response of the Unit 1 control room

operators was very good, with timely'and appropriate response to each alarm.

01.3

Midloo

era 'ons

Unit 2

a.

ns ec ion Sco

e 71707)

b.

The inspectors verified the prerequisites and witnessed the performance of midloop

operations, when Unit 2 was in a reduced inventory condition.

In addition, the

inspectors witnessed training in preparation for this evolution. The inspectors performed

these inspections on February 19 and March 9, 1998, each time the licensee entered

the reduced inventory condition.

Observa ions a d Fin in s

a

I

Midloo

On February 19, 1998, prior to entering midloop operations early in the outage with a

high decay heat load, the inspectors verified the prerequisites for the evolution. This

included plant tours to verify that personnel and equipment were staged to permit

venting of the residual heat removal pumps in the event of pump vortexing. The

inspectors also ensured that no ongoing evolutions that could affect midloop operations

were in progress.

The inspectors concluded that the prerequisites for entering hot

midloop were satisfied.

The inspectors observed the operations briefing for entering midloop. The briefing was

organized, detailed, and focused on safety.

Licensee management was present and

emphasized expectations with respect to safe operations.

On February 19, with Unit 2 in Mode 5, the inspectors observed the control room crew

drain the reactor vessel water level down to 107 feet, midlevel of the reactor vessel

hotlegs, in preparation for steam generator maintenance.

The evolution was conducted

without incident, in a very professional manner.

The inspectors monitored the following

special reactor vessel

refueling level indications and other, special instrumentation:

~

Reactor Vessel Refueling Level Indicating System wide and narrow range

~

LT-954 8 LT-953 normal level indicators

0

~

LI-561 normal level indicator

~

Chart recorders wide and narrow range indicators

~

Chart recorders for pressure relief tank pressure and volume control tank level

The inspectors compared these indications throughout the evolution and they appeared

to be accurate.

Allranges and trends were consistent.

The inspectors also witnessed

the maintenance of midloop conditions and the refillfollowing completion of installation

of the steam generator nozzle dams.

These activities were also conducted

satisfactorily.

'

La e Midloo

On'March 10, 1997, following completion of the steam generator tube inspection and

tube plugging, the licensee reentered midloop operations to remove the steam

generatornozzle

dams.

The inspectors reverified the prerequisites were met. The

inspectors provided continuous coverage during the entire evolution and ensured that

the precautions, limitations, and prerequisites,remained

in effect. The inspectors

observed the control room crew drain the reactor vessel down to 107 feet, which was

completed without incident. The inspectors monitored instrumentation, which appeared

to be tracking satisfactorily.

With the reactor at midloop conditions, the inspectors toured the facilityto assess

the

material condition of the systems used for this evolution.

In the room for residual heat

removal Pump 2-2, the operating pump, the inspectors noted that the overhead trolley

hoist for the pump was not in its normally stowed position and was above the residual

heat removal pump and piping. The inspectors were concerned because the overhead

trolley hoist in the pump room was not seismically qualified, and could possibly impact

the operating residual heat removal pump, instrument tubing, or system piping while in

a reduced inventory condition. The inspectors contacted the shift supervisor, who

directed maintenance personnel to stow and lock the hoist in its proper position.

Engineering determined that the failure to stow the overhead hoist was not a significant

concern because

it was unlikely for a seismic event to result in the hoist chains or hoist

to impact residual heat removal components

in such a way that the system could not

perform its intended safety function. The licensee did not document the

inspectors'oncern

on an action request until March 25, after the inspector continued to question

the licensee on the cause and safety significance of this problem.

Procedure MP M-10.2, "Residual Heat Removal Pump Motor and Impeller Handling,"

Revision 5, Section 7.6.9, required the hoist and trolleys in the residual heat removal

pump rooms to be placed in their normally stowed positions with the chains secured

in

place following maintenance.

Although the licensee believed that this procedure was

properly implemented, the hoist was not in its proper location when required.

On March 25, 1998, the licensee began investigating this problem. The licensee noted,

that although Section 7.6.9 of Procedure MP M-10.2 was not signed off as completed,

-5-

maintenance personnel stated that they had stowed the hoist as required.

The licensee

believed that subsequent

to mechanical maintenance personnel properly stowing the

hoist, other personnel removed the restraining bracket from the chain and moved the

hoist back over the pump. At the end of the inspection period, the licensee had not

determined the cause of the improper hoist location.

The inspectors discussed this issue with licensee engineering personnel.

The licensee

noted that although licensee procedures required plant walkdowns to identify seismic

concerns prior to operational mode changes,

no such requirement existed for entry into

midloop operations in the prerequisites of the midloop procedure.

Procedure OP A:2-III,

"Reactor Vessel - Draining to Half Loop/Half Loop Operations with Fuel in the Vessel,"

Revision 13, was not appropriate to the circumstances.

Specifically,

Procedure OP A:2-IIIdid not provide for verification that no seismic concerns existed

prior to entry into reduced inventory conditions. As a consequence,

the hoist and trolley

for residual heat removal Pump 2-2 was not in its seismically approved storage position

and the chains were not in the storage racks when residual heat removal Pump 2-2 was

being used for decay heat removal. The failure to provide a midloop procedure

appropriate to the circumstances

is a violation of 10 CFR Part 50, Appendix B,

Criterion V (50-323/98007-02).

Co cusions

A violation was identified for failure to provide a midloop procedure appropriate to the

circumstances that specified proper stowage of a nonseismically qualified hoist. The

hoist was left in an unstowed condition above the operating residual heat removal pump

during a reduced inventory condition. Licensee preparations and implementation,

including the operations pre-evolution briefing for early midloop operations, were

conservative and reflected a focus on safety.

Reflood of the Unit 2 Emer enc

Core Coolin

S s ems followin Core Offload Outa

e

Period

Ins ection Sco

e 71707

On March 2, the inspectors observed control room activities while preparations were

made to refill the residual heat removal and other emergency core cooling systems.

On

March 3, the inspectors observed operations venting emergency core cooling systems

using Procedure OP A 2:Vll, "Core Offload Window Systems Restoration," Revision 6.

Observa ions and Findin s

The pretask briefing performed by the shift foreman covered the precautions and

limitations, prerequisites, major steps, individual responsibilities and communications

between organizations.

The personnel attending the briefing included the operators

assigned to perform the venting, operators in the control room, radiation protection

personnel assisting with the venting, and technical maintenance

personnel assigned to

~ 1

-6-

backfill and place into service the reactor vessel refueling level instrumentation system.

Special attention was given in the briefing to maintaining vessel level to avoid cavitation

of the residual heat removal pump. The required positions of the newly installed throttle

valves also received additional attention and were verified to be addressed

by the

procedure.

The control room operators closely monitored reactor vessel level indications and

residual heat removal system parameters

and were cognizant of the field activities

during the filland vent. Good two-part and three-part communications, self checking

and peer checking was observed in the control room throughout the evolution. Venting

of high point vents within controlled surface contamination areas was observed.

The

operators and radiation protection personnel worked well together,to contain the vented

liquid and demonstrated

good radiological practices in entering and exiting controlled

areas and monitoring for contamination.

onctu ions

The reflood of the emergency core cooling systems evolution was well coordinated and

controlled, with the participants aware of their responsibilities. The pre-evolution briefing

was comprehensive, with emphasis on safe, cautious performance and the necessity for

good communications.

~Rf

i Alii

lns ection Sco

e 6071

On March 4 and 5, the inspectors observed refueling activities in the control room, fuel

building and containment.

These activities included handling and movement of the fuel

assemblies

from the spent fuel pool to the upender and from the upender to the final

core location, control room monitoring of required parameters,

and reactor engineering

calculations of inverse count rate ratio and monitoring of fuel location for accountability

requirements.

The inspectors reviewed Operating Procedure OP B-8DS2, "Core

Loading Sequence,"

Revision 20, which contained the procedural requirements for these

activities.

Observatio

s and Findin s

The inspectors observed the refueling senior reactor operator directing the fuel handling

operations in containment.

He was observed to maintain good supervision over the

activities, maintaining communications with the control room and the personnel in the

fuel building, giving directions to the crane operator and other observers, verifying the

correct core location as specified in the fuel movement tracking sheets, monitoring the

load on the manipulator crane as the fuel assembly was raised or lowered, and

confirming the proper indicating lights and Z-Z tape position. The fuel assemblies were

inserted off index as described in the procedure. The inspectors observed the insertion

of an assembly against the baffle and into a three-sided box, which resulted in a rapid

e

-7-

load fluctuation when the assembly bottom nozzle hung on the baNe.

The senior

reactor operator immediately stopped the loading and performed the steps required in

the procedure to protect the assembly and achieve a successful installation. Reactor

engineers were monitoring and video taping the fuel movement with cameras installed

on the upper internals guide pins.

Fuel Handlin

The inspectors observed the movement of the fuel assemblies

in the fuel handling

building. This activity was coordinated with the senior reactor operator to ensure an

assembly was not raised out of the spent fuel racks until the upender was unloaded in

the containment.

The crane operators were observed to followthe procedural

requirements, including observing limitations on crane motion, load, and speeds.

The

fuel assembly location and identification was independently verified against the fuel

movement tracking sheets prior to being removed from the racks.

Reactor engineers

used an underwater camera to monitor and record the fuel assemblies

as they were

moved to the upender.

The inspectors also observed that the foreign material exclusion

area controls around the reactor cavity and the spent fuel pool were effective.

ConroIRoomA

iviies oSu

o

FueILoad

The inspectors observed control room activities in support of fuel load. On March 5,

while inspecting the switch lineup on the nuclear instrumentation panels, the inspectors

noted that the "High Flux at Shutdown" alarm switch for source range Channel N-32 was

in the blocked position, rather than the normal position required for the current step in

the core loading procedure.

This was immediately brought to the attention of the control

operator and reactor engineer in the control room. Operations placed the switch in the

normal position and documented on Action Request A0455551 that OP B-8DS2,

Attachment 9.8, "Fuel Movement Tracking Sheet," required the "High Flux at Shutdown"

alarm for N-32 be restored at Step 21B and this action had been overlooked.

Approximately eight additional assemblies

had been loaded after Step 21B and before

the alarm was returned to normal.

During this time, both channels of source range

nuclear instruments were operable and monitored continuously by the control operator

and reactor engineer.

In addition, one channel of source range was audible in both the

control room and containment, and the "High Flux at Shutdown" alarm for Channel N-31

was in normal.

The failure to restore the "High Flux at Shutdown" alarm at the specified step in the core

loading procedure, Step 21B, is a violation of Technical Specification 6.8.1.a.

(50-323/98007-03).

A contributing cause of the failure to restore the "High Flux at Shutdown" alarm

appeared to be the format of the fuel movement tracking sheets

in that: the applicable

step contained three actions, the actions were to be performed by two different groups,

the step did not have a separate step number (step numbering was used to designate

the number of assemblies

loaded), and the place for date, time, and initials was covered

0

-8-

by the text of the step. Another contributing cause was that the responsibility to perform

the actions was not clearly assigned prior to the evolution.

Reac or En ineerin

Activiies Durin

Fuel Lo d

Step 21B of OP 8-8DS2, Attachment 9.8, contained several actions, including verifying

that the signal-to-noise ratio for source Range N-32 was greater than 2. The procedure

provided no directions for determining signaI to noise ratio. The completion of this

activity was not documented

in the procedure by a separate signature or initials,

although the reactor engineer stated that he had performed the verification. The step

was not signed until after the missed'action of restoring the alarm was brought to the

control operator's attention.

Step 6.17 of OP B-8DS2 stated, in part, that a calculated prediction of critical

assemblies was required to be performed after the first 13 assemblies

had been loaded

adjacent to a detector., The reactor engineers used a computer program to calculate

inverse count rate ratio (ICRR). This program also calculated the predicted ICRR if 12

additional assemblies were loaded based on extrapolation of the most recent ICRR data

points.

Ifthis predicted ICRR were greater than zero, it indicated core load could

continue.

This method satisfied the intent of performing ICRR, but appeared

inconsistent with the procedure in that the number of assemblies

predicted to cause

criticality was not calculated.

Step 6.25 of OP B-8DS2 stated that a fuel accountability audit and a foreign materials

scan at the completion of core loading be performed, prior to placement of the upper

internals in the vessel.

This was to consist of either producing a video tape of the core

and reviewing it for foreign objects, coupled with a verification of proper loading from the

tape, or visual (camera and monitor) verification with two signatures to document the

inspection.

Inspection and verification of nozzle-to-nozzle and nozzle-to-baffle

clearances was also required.

Reactor engineering satisfied the fuel accountability

requirement by reviewing the video tapes made in the spent fuel pool and in the reactor

cavity during fuel loading. Afterthe core was loaded, a video tape was made with a

camera scan to inspect for foreign material and clearances

between the assemblies

and

between the assemblies

and the baNe plate. Although the methods used were

technically adequate,

they did not appear to be entirely consistent with the procedure

(although vague) in that the tape of the core produced during the post core load scan

was not used to verify proper loading, nor was a visual (camera and monitor) verification

with two signatures to document the inspection performed.

The procedure did not

provide guidance nor acceptance

criteria for the size of the gaps between the

assemblies or between each assembly and the baffle. The inspectors also noted minor

documentation discrepancies

in the closeout of the paperwork.

Conclusions

A violation was identified for failure to restore the "High Flux at Shutdown" annunciator

when the required number of fuel assemblies was installed in,the core. The

responsibility to perform the actions was not clearly assigned prior to the evolution. The,

lack of formality in performance of control room refueling activities contributed to the

failure to restore this alarm.

The control of safety activities lacked clear procedural guidance and clear management

expectations.

The lack of procedural guidance for performing signal to noise ratio

calculation, the lack of acceptance

criteria in the procedure for assembly to assembly

and assembly to baNe clearances,

and the confusing procedure format which

contributed to the missed action of restoring the "High Flux at Shutdown," were

weaknesses

in the procedure.

The method used to calculate inverse count rate ratio

and the method used to perform the post core load verification appeared to be

inconsistent with the methods described in the procedure, although the procedure was

vague.

The lack of separate signatures in the controlled copy of the procedure for

verifying that the signal-to-noise ratio was greater than 2 was an example of poor

,

documentation of procedurally required activities.

The necessary

coordination between

the fuel handlers in containment, the fuel handlers in the refueling building, the reactor

engineer, and the control operator's observation of plant conditions were otherwise

performed well.

01.6

Clearance Rela

d

rrors Durin

R8 Refue in

Outa

e

ns

e

ion

co

7 707

The inspectors reviewed the licensee's self-assessment

of operations clearance

performance during 2R8, and 27 action requests initiated to document errors related to

clearances.

b.

Observation

and Findin s

Operations performed a self-assessment

of their performance during 2R8 and

concluded there was a reduction in clearance errors and a reduction in the severity of

these errors compared to 1R8. The licensee categorized the errors by significance. A

level 1 (high significance) error was one that caused or could have caused personnel

injury or equipment damage or all clearance process barriers were breached.

A level 2

(moderate significance) error was one where some clearance process barriers were

breached,

but others prevented placing personnel or equipment in jeopardy. A level 3

(low significance) error was an inconsequential error related to some phase of the

clearance process.

In comparing the performance in 2R8 to 1R8, the licensee

determined there were 3 high significance errors in 2R8 as compared to 8 in 1R8, there

were 15 moderate errors in 2R8 compared to 33 in 1R8, and there were 45 low

significance errors in 2R8 compared to?3 in 1R8.

During 2R8, none of the errors

resulted in personnel injury or equipment damage.

The licensee identified some recurring themes in the clearance errors.

Most of these

themes had minimal significance.

Tags becoming unsecured or becoming illegible but

none of the cleared equipment were operated as a result, and minor administrative

~

~

-10-

errors such as missing a set of initials were considered minor. Errors of most

significance were generally caused by lack of proper self verification and independent

verificatIon.

The most significant clearance errors during 2R8 were related to clearing tags to

perform testing and resulted in tags being removed from the wrong components or

allowing work to be performed without a clearance,

as follows:

On February 25, while attempting to remove a clearance tag from 52-2F-02R.to

allow testing of containment fan cooling Unit 21, an operator mistakenly removed

a tag from 52-2F-01R and attempted to close the breaker, which jammed and did

not close.

The operator rec'ognized his mistake while showing the technical

maintenance technicians the jammed breaker (AR A0454479):

~

On February 26, while processing a partial removal of a clearance to perform

testing, a senior control operator marked the desired return to service position on

two incorrect clearance points. As a result, an operator removed tags and

closed two incorrect breakers.

The problem was identified and the breakers

reopened and retagged (AR A0454548).

~

On March 17, after testing of a control rod drive mechanism fan for proper

rotation identified the fan motor leads needed to be swapped; the power supply

breaker was opened and technical maintenance swapped the leads without

clearing the breaker (AR A0457998).

Other clearance errors had the potential to be cause equipment damage or personnel

injury, but were identified outside the clearance process.

For example,

On March 4, while removing tags following work, a senior control operator

discovered a caution tag hanging over the fuse holders for fuses that had been

removed for Valve RCS-2-PCV-474.

This tag should have removed the fuses for

Valve RCS-2-PCV-472 (AR A0455485). This error was not identified in the

clearance process.

On February 17, Clearance 57169 was hung prior to the proper plant conditions

being established,

isolating reactor coolant pump seal injection while the reactor

coolant system pressure was approximately 350 psig. Operating procedure

OP A-6:II, "Reactor Coolant Pumps - Shutdown and Clearing," Precautions and

Limitations 5.2, specified that seal injection should remain in service as long as

the reactor coolant system is pressurized to prevent introduction of crud from the

reactor coolant system into the seals.

The control room operators, responding to

the loss of seal injection, contacted the operator in the field, and the seal

injection flow was reestablished

(AR A0455670). This clearance error was not

found in the clearance process, but by alarms in the control room.

-11-

On March 3, workers detected voltage on a cathodic protection circuit prior to

performing work. The clearance, 56570, did not clear an alternate source of

power from Unit 1's power supply 52-P J18-1-33 (AR A0455394).

Other clearance errors were considered moderately significant by the licensee because

not all barriers were broken, such as the errors were identified during walkdown by

maintenance prior to starting work. These errors indicated that improvement in self-

verification in the operations organization required improvement, because

more than

one barrier failed. For example:

On February 16, during the'maintenance

walkdown, Breaker 52-23J-08 was

found closed with a man-on-line tag hanging requiring the breaker to be open

(AR A0453258).

On March 6, during a clearance walkdown prior to starting work a man-on-line

tag was found hanging on the wrong fuse. The tag was hanging on the fuse

holder for lYFW21, but it should have been hung on the fuse holder for lYFW22,

which was the cross feed power from the relay scheme for lYFW21

(AR A0455669).

Several other less significant errors existed that were identified by the independent

verifier, thus indicating a failure of only one barrier.

The inspectors noted that, fortuitously, none of these examples of clearance errors

resulted in personnel injury or equipment damage; however, the potential existed.

Multiple failures of operations personnel to properly implement the clearance procedure

is a violation of Technical Specification 6.8.1.a (50-275;323/98007-04).

c.

Conclusions

'

violation was identified for several examples of failure to properly implement the

clearance procedure.

Several significant errors were not found or prevented by the

clearance process and resulted in work being performed or had the potential for work to

be performed without the required isolation from sources of energy to allow safe work.

However, the number and significance of clearance errors in Refueling Outage 2R8

were improved over previous outages.

02

Operational Status of Facilities and Equipment

02.1

Chemical and Volume Con rol S stem Lea

a.

ns ectio

co

e 93702

On February 13, 1998, the inspectors responded to the control room and observed

operator response to a leak from the chemical and volume control system.

0

b.

Observa ionsa dFindin s

On February 13, 1998, while Unit 2 was operating at 100 percent power, the control

operator identified that volume control tank level was dropping at a rate of approximately

12 gallons per minute.

Operators implemented Procedure OP AP-17, "Charging Line

Leak at Power," Revision 19, and isolated the flowpath to the deborating demineralizer,

but volume control tank level continued to drop at the same rate.

Approximately 30

minutes later a nuclear equipment operator reported that the miscellaneous equipment

drain tank level was rising. The shift foreman directed that the nuclear equipment

operators check the flow sight glasse's

in the auxiliary building, which determined that

Flow Indicator Fl-276 had flow. The nuclear equipment operators verified the position of

check valves that drain through Flow Indicator Fl-276. A nuclear equipment operator

found that Valve CVCS-2-66 (the centrifugal charging pump recirculation drain line

isolation valve) was approximately 1-1/2 turns open.

The valve was closed, which

stabilized volume control tank level. The inspectors monitored the operator response to

the event and considered the operator resolution of the lowering of volume control tank

level to be timely and thorough.

Licensee investigation revealed that maintenance personnel performed penetration seal

work in the overhead area above Valve CVCS-2-66, and that the likely cause of the

event was that the handwheel for Valve CVCS-2-66 was bumped while using a ladder

adjacent to the valve. The inspectors noted that NRC Inspection

Report 50-275; 323/97019 discussed an event in which the root cause was similar. In

the previous event, maintenance personnel stepped on a main steam isolation valve

limitswitch when working overhead that resulted in a reactor trip and safety injection.

In response to this event, licensee management

issued a shift order to the crews

describing the event and directing operators to brief maintenance personnel on sensitive

equipment areas while working overhead.

In addition, licensee management issued a

memorandum to all employees that discussed the event and the need to exercise

vigilance in ensuring that care is taken not to disturb equipment while working in the

plant. The inspectors considered the licensee actions appropriate.

Conclusions

Maintenance personnel did not exercise appropriate care during penetration seal work

and stepped on a valve handwheel.

This challenged operators by causing a leak in the

chemical and volume control system.

Operator response to decreasing volume control

tank level was timely and thorough.

)

-13-

03

Operations Procedures and Documentation

03.1

idloo

Abnormal 0 era in

rocedures

a.

Ins

c ion Sco

71707)

The inspectors evaluated the licensee's response to Action Request A0451605, which

identified an inadequate pressure rating of the reactor vessel refueling level indicating

system.

b.

Observ

io s and Find'n

s

In 1993, the licensee upgraded their strategies for responding to abnormal events during

shutdown conditions.

This item was done with the help of the vendor. These strategies

were incorporated into Procedure OP AP SD-O,."Loss of, or Inadequate Decay Heat

Removal," Revision 3.

New strategies for combating casualties during shutdown and midloop operations

included the use of natural circulation cooling and reflux cooling. Each of these methods

required pressurizing the reactor coolant system to up to 400 psig and rejecting heat

through the secondary side of the steam generators.

However, on January 23, 1998, during simulator training in preparation for midloop

operations, the licensee noted that the reactor vessel refueling level indication system,

predominantly constructed from tygon and nylobraid tubing, was designed for a normal

operating pressure of 57 psig. The burst pressure of the reactor vessel refueling level

indicating system was 150 psig for temperatures

expected to be encountered during

these abnormal procedures.

Therefore, although Procedure OP AP SD-0 directed the

operators to pressurize the reactor coolant system to 400 psig in the event of a loss of

decay heat removal, the reactor vessel refueling level indication system was not

designed nor qualified for this pressure.

This condition existed for both Units 1 and 2,

and was of immediate concern for Unit 2 because of the forthcoming refueling outage.

The licensee initiated Action Request A0451605 to enter this item into the corrective

action system.

The licensee evaluated several options to address this condition. Options that were

initiallyconsidered included allowing the system to rupture and making up with safety

injection or entering containment and isolating the level indication system following a

loss of decay heat removal. The licensee determined that these solutions were

undesirable because each involved a loss of level indication during midloop operations

and would further complicate an event.

The licensee chose to upgrade the system to

withstand pressures

of up'to 250 psig by replacing the tubing with stainless steel and

installing valves with a high pressure rating. To accomplish this task, the licensee

initiated Design Change Package DCP J-50422 to upgrade the system.

In addition,

Procedure OP AP SD-0 was revised to limitpressurization of the reactor coolant system

t

-14-

to 250 psig. This modification was completed on February 17, and the system was

placed in service for midloop operations on February 19. The inspectors noted that the

upgraded reactor vessel refueling level indicated system performed satisfactorily during

both entries into midloop operations for Unit 2.

The inspectors noted that the apparent cause of this issue was the failure of operations

. procedure preparers and reviewers to recognize that the reactor vessel refueling level

indication system was not qualified for the pressures

specified in the proposed

strategies for mitigation of a loss of decay heat removal.

Both the preparer and the

reviewer of Procedure OP AP SD-0 were operations personnel that were not

knowledgeable of the system's design basis.

The licensee's quality assurance

plan only

required the licensee to make a determination ifa cross-disciplinary review was required

for any new procedures.

The licensee determined that such a review was not required

for Procedure OP AP SD-0. Therefore, Procedure OP AP SD-05 was not reviewed by

design or system engineers to ensure that the systems affected by the new procedure

were designed to withstand the referenced conditions.

This condition existed for

approximately 4 years and encompassed

several refueling outages for both units when

the conditions that could potentially use Procedure OP AP SD-0 were in place. This

issue was mitigated by the fact that a safety injection pump was available during

midloop operations and could have adequately made up coolant inventory to the core in

the event of a reactor vessel refueling level indication system rupture.

The inspectors reviewed the proposed corrective actions for AR A0451605 and noted

'hat

these actions included upgrading the reactor vessel refueling level indication

r

system, revising procedures and drawings to reflect the modification, and performing a

maintenance preventable functional failure evaluation.

These corrective actions were

proposed by February 27. At the end of the inspection period (Nlarch 28), no further

corrective actions were proposed.

Based on the above discussion of the apparent cause of the problem, the inspectors

concluded that corrective actions did not address the failure of the procedure

preparation and approval process to identify the need to upgrade the reactor vessel

refueling level indication system or the need to choose another mitigation strategy.

Because of the incompleteness

of the corrective actions, the exercise of discretion was

not considered warranted.

The failure to properly translate the design of the reactor vessel refueling level indication

system into Procedure AP SD-0 is a violation of 10 CFR Part 50, Appendix B, Criterion

III (50-275;323/9800?-05).

Conclusions

A violation was identified for failure to translate the design of the reactor vessel refueling

level indication system into abnormal operating procedures.

The licensee exhibited

good attention to detail in identifying this issue during simulator training. Corrective

actions for this violation failed to address deficiencies in the procedure preparation and

l

-15-

approval process.

05

Operator Training and Qualification

05.1

Uni 2 Ou

e Traini

s eci

Sco

e 7 707

The inspectors observed training in preparation for the shutdown and anticipated hot

midloop evolutions.

Observa ions

nd

indin s

From February 10 to 13, 1998, the inspectors observed both classroom training for the

Unit 2 shutdown and hot drain down to midloop evolutions. This training included both

classroom and simulator scenario sessions for the two expanded crews that were

anticipated to perform these evolutions.

System engineers that would be performing

tests during the evolutions were involved in order to anticipate any impact on plant

activities that the tests might have.

The inspectors noted valuable lessons learned and

procedural changes that were identified during the training and that, in particular, the

simulator training was professional and well executed.

The licensed operators and shift

engineers viewed their training to be valuable and would ensure successful performance

of the planned shutdown evolutions. The inspectors noted the actual observed

evolutions 'were implemented without major incident. The inspectors also determined

that the involvement of the test engineers with the crew training was a valuable

contribution to the outage and was an improvement over the training provided in the

past.

Evidence of the value of this training was exhibited by the identification that the

reactor vessel refueling level indication system was not designed for pressures

required

in the abnormal operating procedures.

Co cusions

The training provided for Unit 2 outage preparation was implemented well and provided

valuable lessons learned and necessary

procedural changes.

The inspectors noted, in

particular, that the simulator training was professional, well executed, and identified a

vulnerability in the abnormal operating procedures.

II. Maintenance

M1

Conduct of Nlaintenance

M1.1

Main enance Observa ions

a.

Ins ec ion Sco

e 62707

The inspectors observed portions of the following work activities:

b

-16-

MP M-7.53, Reactor Coolant Pump Motor Ten (10) Year Inspection for Reactor

Coolant Pump 2-1

. Replace Flow Element FE-974 in the Safety Injection to Loop 1 Cold Leg, Work

Order C0153639

Replace Flow Element FE-975 in the Safety Injection to Loop 2 Cold Leg, Work

Order C0153640

Replace Existing Grating at Residual Heat Removal Sump for 2R8, Work

Order C0154660

Install Ground Buggy in Cubicle for Component Cooling Water Pump 1-1.,

MP E-7.11B, Revision 17, for Clearance CL 00057211,

Preventative Maintenance on Auxiliary Feedwater Pump 1-2, Work

Orders R0161465 and R0170439

Remove and Replace Valve FW-2-1 83, Work Order C0144622

Remove and Replace Gasket on Piping Flange Downstream of Containment

Spray Pump 1-2 Vent Valve CS-1-24,

Work Order C0156657.

Sample Containment Spray Pump 1-2 Pump Bearing Oil, Work Order R0178536

Sample Containment Spray Pump 1-2 Motor Bearing Oil, Work Order R0170178

Perform Motor Preventative Maintenance on Containment Spray Pump 1-2,

Work Order R0162541

b.

Ob e

a ions and Findin s

On March 2, the inspectors observed portions of the 10-year inspection of the reactor

coolant Pump 2-1 motor. The technicians had the work package at the job site and

were performing the steps as written. The torque wrench used was calibrated and had

the proper range as specified in the procedure.

An alternating pattern was used to

tighten the bolts, performing three passes with increasing torque values.

The inspectors observed the replacement of Flow Elements FE-974 and -975 in the

safety injection lines to the Loop 1 and Loop 2 cold legs. A radiological catch bag, tube

and bottle were setup on each line to contain the contaminated water released when the

flanges were unbolted. This arrangement was effective in controlling the spread of

contamination.

Scaffolding to support the work was properly erected and had the

required inspection tags attached.

A nuclear quality services inspector was observed

verifying the gasket, all-thread, nuts, bolts, lubricant and new orifice plates were as

specified in the work package.

The nuclear quality services inspector also verified the

~

~

-17-

orientation of the new orifice plate was correct for the direction of flow and matched the

orientation of the old orifice plate.

The inspectors observed the modiTications made to the Unit 2 residual heat removal

containment recirculation sump and inspected the final configuration after the new

screens were installed.

Cutting, grinding, and welding on the structure were properly

controlled, with the required posting of permits for open flame and combustibles, and fire

watches in place.

The modifications appeared to be effective in closing all the paths for

small debris to enter the sump.

New flashing installed around the grating was effective

in closing the gaps between the grating and the sump housing.

The design change is

described in Section E2.1 of this repo'rt. During the inspection of the inside of the sump,

the inspectors noted no debris or peeling paint inside, the condition of the sump housing

appeared sound, with sufficient structural support, a secondary internal screen that

covered the inlets to the suction piping, and no visible unscreened

path into the sump.

On March 3, the inspectors observed the installation of a ground buggy in the cubicle for

component cooling water Pump 1-1 for maintenance.

The maintenance personnel

installing the ground buggy were knowledgeable of the equipment, and the correct

method and indications of proper alignment of the buggy in the cubicle. They were

aware of the required safety precautions,

using flash suits, ensuring all unnecessary

personnel were out of the room, ensuring the doors were posted to prevent entry, and

using a voltage tester to confirm the load side of the breaker cubicle was deenergized.

They inspected the ground buggy to verify correct configuration and current rating. An

operator was also present to verify the correct breaker cubicle, correct ground buggy

configuration (line side or load side), and correct current rating. Both the operator and

the maintenance personnel had their procedures at the job site and used them. The

ground buggy was installed without difficulty.

The inspectors observed the removal and replacement of flanged butterfly

Valve FW-2-183, auxiliary feedwater Pump 2-3 suction isolation valve. The alignment of

the auxiliary feedwater pump to its motor was monitored during the loosening of the

bolts and removal of the valve to ensure the suction pipe was not exerting excessive

load on the pump suction. The alignment was rechecked following installation of the

new valve. The maintenance personnel had the procedure at the job site and used it

correctly. The torque wrench was within its calibration. The clearance for the work,

C0144622, was verified by the inspector to be hung and to adequately protect the

equipment and personnel.

On March 19, the inspectors observe performance of routine maintenance

on

containment spray Pump 1-2 by technical maintenance and mechanical maintenance.

This work included obtaining samples of motor bearing oil and pump bearing oil,

replacing a gasket on a pipe flange downstream of the pump vent valve, and routine

cleaning, inspecting, and testing of the motor leads and junction boxes.

A radiation

protection technician assisted

a mechanic in removing and replacing the pipe flange

gasket.

A catch bag, tubing, and bottle were erected prior to opening the flange to

contain any liquid. Good radiological practices were used to survey the parts and

0

-18-

equipment and to minimize the contamination released by the work. The survey

equipment and torque wrench were inspected arid found to be within calibration. The

new gasket material was verified to match that specified in the work package.

The

flange bolts were observed to be torqued to the value specified in

Procedure MP M-54.1.

The oil samples were obtained as specified in Procedure MP M-56.7, "Lubricant

Sampling." The oils used to refill the bearings were verified to agree with the lubricant

charts contained in Procedures

MP M-56.24 and E-56.1, and to agree with the

nameplates

mounted on the containment spray pump. The electricians cleaning and

inspecting the motor leads and junction boxes were thorough, and checked the torque

on the bolted connections using a torque wrench of the proper range and within its

calibration frequency.

One bolt that appeared to be corroded was removed, cleaned,

inspected, and reinstalled after its condition was determined to be acceptable.

The

clearance for this work, CL0057967, was reviewed and found to be adequate to protect

the work and each tag was hung in the correct location.

c.

Conclusions

A number of maintenance activities were observed and were performed in accordance

with the procedural requirements.

Good coordination between technical maintenance,

mechanical maintenance and radiation protection was observed in performing several,

maintenance tasks concurrently on the containment spray pump; thereby reducing the

time the pump was inoperable due to maintenance.

M1.2

S

eillance Observ

io s

s ec ion Sco

e

172

Selected surveillance tests required to be performed by the Technical Specifications

were reviewed on a sampling basis to verify that:

(1) the surveillance tests were

correctly included on the facility schedule; (2) a technically adequate procedure existed

for the performance of the surveillance tests; (3) the surveillance tests had been

performed at a frequency specified in the Technical Specifications; and (4) test results

satisfied acceptance

criteria or were properly dispositioned.

The inspectors observed all or portions of the following surveillances:

STP M-13F

4KV Bus F Non-Sl Auto -Transfer Test, Revision 22

STP M-15

Integrated Test of Engineered Safeguards

and Diesel Generators,

Revision 29

STP R-6

Low Power Reload Physics Tests,

Revision 7

STP R-30

Reload Cycle Initial Criticality, Revision 12

-19-

STP R-31

Rod Worth Measurements

Using the Rod Swap Method,

Revision 8

STP M-120

Firewater Availabilityto Centrifugal Charging Pump Coolers,

Revision 2

The inspectors also reviewed the results of the following surveillances:

STP R-17

Estimated Critical Position;

Revision 12A

STP G-8C

'perational Checkout of the Reactivity Computer, Revision 7

STP R-7A

Determination of Moderator Temperature Coefficient, Revision 10

b.

Observa ions and Findin s

On February 24, the inspectors observed the performance of surveillance test procedure

(STP) STP M-120, "Firewater Availabilityto Centrifugal Charging Pump Coolers,"

Revision 2, on the Unit 1 centrifugal charging pumps.

This test demonstrated

the ability

to flow cooling water through the hoses and manifold to provide. cooling to either

centrifugal charging pump using firewater. Firewater would be used in the event

component cooling water was lost to both centrifugal charging pumps.

The operators

had the procedure and signed offthe steps as they were performed.

Allof the hoses,

fittings and manifold worked as design with no observable leakage.

The test adequately

demonstrated that the equipment could be properly installed and would provide cooling

'ater

to the centrifugal charging pump cooling piping. The operators performed self

checking and independent verifications, by verifying the valve numbers on the tags

matched the procedure prior to operating the valves.

The operators were careful to

cleanup the small amount of water that spilled during the disconnection of the hoses.

On March 15, the inspectors observed the pretest briefing and performance of

surveillance test procedure STP M-13F, "4KVBus F Non-Sl Auto-Transfer Test." The

pretest briefing was comprehensive,

covering precautions and limitations, prerequisites,

communications and responsibilities, major test evolutions, and expected results.

The

performance of the test was well coordinated, with clear communications between the

test personnel and control operators, including 3-part communications.

During the test,

all equipment operated as expected and the test results satisfied the acceptance

criteria.

On March 17, the inspectors observed the pretest briefing and performance of

surveillance test procedure STP M-15, "Integrated Test of Engineered Safeguards

and

Diesel Generators."

The pretest briefing was comprehensive,

covering precautions and

limitations, prerequisites, communications and responsibilities, major test evolutions,

and expected results.

Several other surveillance requirements were satisfied

concurrently with this test, including STP V-11, "Containment Isolation Phase

B

0

-20-

Valves FCV-355, FCV-356, FCV-357, FCV-363, FCV-749, and FCV-750." The

inspectors observed good communications and coordination between test participants,

which was necessary to capture the starting time of the many different pumps and fans,

and to coordinate the recording of data from control board meters. During the test, the

newly installed load tap changer for the startup transformer was used per the operations

procedure to transfer the vital buses from startup to auxiliary power.

On March 24, the inspectors observed the preparations for and achievement of initial

criticality and performance of low power physics testing. A pretask briefing was

performed by the shift foreman and reactor engineer.

Management oversight was

provided during the briefing and evolution by the engineering services manager.

The

briefing covered responsibilities and communications, Technical Specification

requirements,

including the special test exceptions and related surveillances,

precautions and limitations, prerequisites,

and brief description of the physics tests.

The

prerequisites were verified by the inspectors.

Operations limited other plant activities

that could cause distractions to the control room or unnecessary

alarms during the

physics testing.

Communications between the reactor engineers and the control operators were clear

with 3-part communications consistently used.

The reactor engineers were

knowledgeable of the test requirements and test equipment.

They continually evaluated

the data against expected results and made conservative decisions in implementing the

procedures.

The approach to criticalitywas performed slowly and cautiously, with

criticality achieved well within the allowed deviation from the estimated critical

conditions.

The control operators maintained the plant stable to ensure good data for

the reactor physics tests.

The test results met both the acceptance

criteria and review

criteria.

Conclusions

The inspectors observed a number of surveillance tests and found that the surveillances

observed were performed in a cautious manner with self-checking and proper

communications employed.

The procedures governing the surveillance tests were

technically adequate and personnel performing the surveillances demonstrated

an

adequate

level of knowledge.

The inspectors noted that test results appeared to have

been appropriately dispositioned.

M1.3

Con ainment In

e

ion Prior

Close

u for Con ainment In e

ri

lns ection Sco

e

6 707

The inspectors toured containment during the period when containment work activities

were finishing and efforts to clean up in preparation for containment closure were in

progress.

-21-

Observa 'ons and Findin s

The cleanup effort was well organized with coordination between completion of the final.

work activities, surveying and decontamination of radiologically controlled areas,

removal of equipment, tools, and supplies, as well as cleaning to meet housekeeping

standards occurring simultaneously.

Loose insulation buckles had been a concern in

the previous outage and were addressed

early in the cleanup schedule.

The inspectors

found no unfastened,

broken or missing insulation buckles during their tour. The reactor

coolant pump oil collection system was inspected and found to be properly assembled.

The various sections were bolted or fastened into place.

The joints between the

sections were sealed with approved sealant.

The oil collection tank was inspected and

found to be clean and empty of oil. The inspectors noted several small bolts and nuts

and other debris.

These were identified to the licensee and removed.

The inside of

several mechanical panels were inspected and found to be in good materiel condition

with no housekeeping

problems.

Radiologically contaminated material was properly

separated from noncontaminated

material and appropriately labeled and posted.

Conclusions

The containment cleanup and closeout activities were appropriately controlled, and the

material condition of containment areas was satisfactory for restart of Unit 2.

Maintenance and Materiel Condition of Facilities and Equipment

eview of Pa

Len th Control Rod Drive Mechanis

s Transi ion Weld

Unit 2

Ins ection Sco

e 62707

The inspectors reviewed the ultrasonic examination of the transition welds on the part

length control rod dive mechanisms to find ifthe same problem found at Prairie Island

Unit 2 existed at Diablo Canyon.

Observa ions and Findin s

Prairie Island Unit 2 shut down on January 24, 1998, because of reactor coolant system

pressure boundary leakage.

The licensee estimated the leak rate to be 0.2 gallons per

minute as measured

by mass balance calculations and radiation monitors.

On

February

27, 1998, Northern States Power reported to the NRC that one of four part

length control rod drive mechanisms,

G-9, had a leak in the lower transition weld of the

motor tube.

The part length control rod drive mechanism had, by design, a section of the pressure

boundary motor tube made of 403 stainless steel.

This design by the vendor allowed

motor coils to be located outside the pressure boundary because

magnetic fields can

penetrate 403 stainless steel.

The rest of the motor tube assembly consisted of 304

~

~

-22-

stainless steel.

To weld the two different stainless steels together, the manufacturer

layered or buttered the 403 stainless with 309 stainless steel. A final weld consisted of-

308 stainless steel and, normally, the stator shroud assembly covered these welds

during operation.

At Prairie Island, the G-9 motor tube had a manufacturing defect in

the buttering weld. The manufacturing defect was a circumferential crack with a high

temperature oxide layer and no evidence of operational extension.

The crack was

almost 360 degrees,

initiated on the inside diameter and opened to the outside diameter

for about /~ inch. Northern States Power concluded that this was a hot crack induced

during manufacturing welding with no sign of propagation during service.

Diablo Canyon had eight part length control rod drive mechanisms and was similar to

Prairie Island. The licensee modified one part length control rod drive mechanism at

Diablo Canyon to be a head vent. The vendor ultrasonically inspected the remaining

seven for the Diablo Canyon licensee.

The vendor completed a hot cell inspection of

G-9 plus other motor tubes from Prairie Island and used the same basic technique at

Diablo Canyon.

Diablo Canyon motor tubes contained the same heat of buttering

material as G-9. One motor tube (M-6) had been weld repaired during manufacturing

similar to the manufacturer repair of G-9. Just as the Prairie Island motor tubes, Diablo

Canyon welds were both penetrant and radiographically tested after buttering and also

final welding.

The ultrasonic testing of seven of the eight motor tubes done by the vendor was a

remote automated inspection with a customized clamp and track for the search unit and

bubbler to supply the water couplant.'he vendor did a '/~ vee inspection with a 1/4

inch, 4 MHZsearch unit using a 45 degree refracted longitudinal wave for the lower

transition weld where the thickness was approximately .400 inches.

A 45 degree

2.25 MHZ, shear wave inspection done on the lower transition weld was not as

informative as the 45 degree refracted longitudinal wave inspection.

The upper weld

where the thickness was approximately .490 inches, used a 60 degree, refracted

longitudinal wave. The technique and personnel were Electric Power Research

Institute

(EPRI) qualified for intergranular stress corrosion cracking ultrasonic testing, and were

in accordance with Procedure DC-800-001, and Field Change Notice Number 1. Also

the technique and equipment was reported to have been used for the "Performance

Demonstration Initiative."

The vendor calibrated the system on two mockups of the motor tube as calibration

blocks, one for the lower transition weld and one for the upper transition weld. Each

calibration block had 0.030 notches on the inside diameter placed at the location of the

buttering weld. These notches gave some measure of the minimum detection limitof

thesystem.

The vendorusedA,

B, and C-scandisplaystoanalyze

theresults.

The

scans showed low intensity noise reflectors from the grain structure of the weld metal,

but did not show any reflectors like that found in G-9.

The inspectors reviewed all the ultrasonic data collected on the lower and upper

transition welds of the seven motor tubes inspected and the manufacturing records.

The inspectors reviewed the calibration records of the lower transition welds. The

-23-

inspectors witnessed the calibration and inspection of four upper transition welds. The

tapered geometry and an outside diameter offset (.010 inches) on the motor tube in the

areas in question presented technique challenges.

The inspectors verified the

inspection of the areas in question.

The calibration notches of 0.30 inches were

discernable and the inspectors found no apparent defects.

Conclusio

s

The license's approach to the inspection of part length control rod welds was sound and

aggressive. The inspectors found the ultrasonic testing showed the seven motor

tubes'pper

and lower transition welds were free of the same kind of defect found at Prairie

Island on the G-9 motor tube.

M4

Maintenance Staff Knowledge and Performance

M4.1

Grou d'Bu

s alla ion Unit 2

The inspectors reviewed the circumstances

surrounding a failed attempt to install a

ground buggy in safety-related 4160 vac Cubicle 52HG5.

b.

erva ions and Find'n s

On February 24, 1998, two contract technicians attempted to install a ground buggy on

the deenergized

line side of a diesel generator load in safety-related 4160 vac

Cubicle 52HG5 in Unit 2 in accordance with Procedure MP E-57.11B, "Protective

Grounding," Revision 17. The bus side of Cubicle 52HG5 remained energized with

4160 vac to provide power to other loads.

Unit 2 was defueled at the time. When the

technicians installed the ground buggy, they inserted the buggy into the cubicle until it

was mechanically stopped.

However, the buggy was hitting an obstruction and was not

fullyinserted into the cubicle.

The technicians began raising the ground buggy to mate with the cubicle line side stabs,

however, because the ground buggy was not fully installed, it began to tiltforward. The

technicians attempted to stop the elevator motor, which continued to run. The

technicians then pulled the power plug to the motor, stopping the lift.

The ground buggy was found to have partially raised and tilted forward, opening the

switchgear shutters and exposing the cubicle bussing.

Because of the forward tilt of the

buggy, the ground buggy stabs were almost touching the energized bus side stabs,

which would have hard grounded the energized 4160 vac bus, challenged switchgear

protective devices, and could have caused significant damage to the switchgear and

injury to the technicians.

The licensee successfully lowered the ground buggy from its

improper position, and after inspection of the cubicle, installed another ground buggy.

-24;

The licensee found that the wheel runners on the original ground buggy were

misaligned, which allowed the buggy to jam inside the cubicle prior to being fully

inserted.

The licensee issued instructions to inspect and repair all 4160 vac ground

buggies for alignment and added this instruction to preventative maintenance

requirements for the ground buggies.

The inspectors noted that Procedure MP E-57.11B and other associated

licensee

procedures did not provide any instructions on how to rack in ground buggies or how to

verify proper installation prior to lifting. Licensee personnel stated that detailed ground

buggy installation instructions had been provided after a ground buggy error in 1995

= caused failure of the Unit 1 AuxiliaryTransformer 1-1, as discussed

in Inspection

Report 50-275; 323/95-017.

Subsequent

to that time, specific instructions for,ground

buggy installation had been removed from Procedure MP E-57.11B, because the

installation was considered by the licensee to be within the skill of the craft.

However, the inspectors noted that the improper installation was accomplished by

contract personnel.

The licensee stated that the two contract technicians were qualified

by licensee training procedures to install ground buggies.

The licensee provided the

training records to the inspectors.

The inspectors noted that these two contract

employees had been certified as having the required training during previous outages

and had received no additional training for this outage.

The licensee stated that the site

program for training of personnel for craft work, including ground bug'gy installation, did

not require periodic retraining for permanent or contract personnel.

In addition, the

licensee's craft procedures did not require that permanent personnel accompany

contract personnel during performance of any work the contract personnel were

qualified for.

The licensee issued additional instructions for installing ground buggies.

The inspectors

questioned whether it was appropriate to give contract personnel, who may have

recently worked at other sites with different hardware, permanent qualification for Diablo

Canyon.

The licensee's evaluation of the event, Quality Evaluation Q0012011, stated

that the corrective action for the installation problem would include a review of the

policy for permanent qualification of contract personnel.

This review willidentify specific

qualifications that willrequire remediation of contractor qualifications prior to performing

the task, based on criteria such as safety significance and frequency of prior use.

The

inspectors considered that the licensee's corrective actions were adequate.

The inspectors considered that Procedure MP E-57.11B was not appropriate to the

circumstance in that the licensee allowed permanent qualification of contract personnel,

allowed these contract personnel to work on safety-related equipment without

supervision, and these contract personnel did not have the necessary

skill of the craft to

successfully complete the work.

The inspectors reviewed the licensee's corrective actions for previous violations for

failure of maintenance

and operations personnel to follow procedures for removal of a

ground buggy in 1995, as discussed

in NRC Inspection Report 50-275; 323/95-017.

~

4

-25-

The inspectors considered that the February 24, 1998, installation problem did not result

from inadequate corrective actions for the previous violations.

In the February 1998

error, both operations and maintenance personnel had followed licensee procedures.

In addition, the inspectors considered none of the previous violations concerned

inadequate procedures or craft skills.

Therefore, since the improper installation of the ground buggy did not result from

inadequate corrective actions from previous violations, this self-revealing and corrected

violation is being treated as a noncited violation, consistent with Section VII.B.1 of the

NRC Enforcement Policy (50-323/98007-06).

Conclusions

A noncited violation was identified for failure to provide a procedure appropriate to the

circumstances for ground buggy installation. The improper ground buggy installation

had the potential to have caused significant damage to safety-related equipment and

injure workers.

Miscellaneous maintenance

Issues

0 en Viola ion 50-27

323/96014-03

failure to remove action request tags from the

control boards.

This violation involved five examples of failure to remove stickers from

the control boards following correction of the deficiencies.

The root cause of this

violation was that no formal program existed to control these action request stickers.

As

corrective action, the licensee: (1) performed an audit of both Units 1 and 2 control

boards to ensure that all control board action request stickers were in place and those

that were resolved had been removed, (2) reprogrammed the plant's computer work

management system such that the status of installation and removal of the control board

action request stickers was tracked and such that the work order could not be closed out

without removal of the stickers, (3) revised procedures for controlling control room action

request stickers to clarify management's

expectations,

and (4) issued a memorandum

that indicated its expectations for supervisory personnel and its intention to hold

personnel accountable.

The inspectors reviewed documentation that verified that these items were completed.

The inspectors noted that Procedure OP2.ID2 "Problem Identification and Resolution-

Action Requests" was revised to state that personnel

~ma

enter "Y" in the action

request sticker removal block in the licensee's plant computer to signify that the stickers

were removed from the control boards.

The inspectors concluded that this procedure

revision did not fullyaddress the corrective actions because

it did not appear to

proceduralize the committed actions such that personnel could be held accountable.

On March 19, 1998, the inspectors performed an audit of existing control board action

request stickers to verify the effectiveness of corrective actions.

The inspectors

identified a total of six discrepancies

between the licensee's existing list of control board

action requests and the stickers on the panels, as listed below:

-26-

The inspectors identified three control board action request stickers on the

panels that were not being tracked in the licensee's computer data base as

control board deficiencies.

The inspectors noted that the existing process in the

licensee's computer data base would remove these stickers.

The inspectors identified one control board action request sticker that was left on

the panels for completed work and was faded such that the problem described

on the stickers was illegible.

The inspectors identified that the computer status block for removal of the control

board sticker for Action Request A0437900 was changed to "Y,"despite the fact

that the sticker was still in place and the problem was not corrected.

The inspectors identified one instance in which an action request was open for a

control board action request, the work was not complete, yet the sticker was

removed.

The inspectors informed the technical maintenance foreman, who corrected the

discrepancies

in the licensee's control board action request tracking system.

The inspectors concluded that the corrective actions for Violation 50-275;323/96014-03

were specifically directed to ensuring that control board action request stickers were

removed when the work was complete, but did not appear to fullyaddress the need to

closely control these deficiency tags. The licensee's programs to ensure that the control

board action requests stickers reflected the licensee's tracking list and the up-to-date

plant configuration warranted further licensee attention. The licensee implemented the

control board action request program to inform operators of equipment that was

deficient, and with inaccuracies

in the program, the operators could be misled.

'ecause

of the additional deficiencies identified with the program,

Violation 50-275;323/96014-03 willremain open for further inspector review of licensee

improvements to the control of control board action requests.

E2

Engineering Support of Facilities and Equipment

E2.1

Residual Heat Removal Recircula ion Containment Sum

Gratin /Scree

M difica ions

a.

lns ec ion Sco

e 37551

The inspectors reviewed Design Change Package DCN N-050317, Revision 0, and the

related licensing basis impact evaluation and screens,

Final Safety Analysis Report

Update Change Request, and field changes.

The inspectors also observed the

modification work in progress and inspected the sump upon completion of the

modiTication..

Nl

4

-27-

b.

Observations a

d Findin s

As the result of the potential to pass debris through the previously installed containment

sump screen and grating that could cause blockage of flowthrough the safety injection

lines, modifications were made in refueling outage 2R8 to reduce the size of the screen

openings from 3/16 inch to 1/8 inch. This modification was made in addition to

emergency core cooling system injection line modifications (DCP N-50286) that

increased the minimum openings in the flow paths.

These modifications removed the

physical'possibility of debris entering the emergency core cooling system that could

block the throttle/runout valves in the safety injection flow paths.

The design change evaluation identified the applicable design bases and design inputs

affected by the modification. The technical review portion of the evaluation confirmed

the sump would meet its design function following implementation of the modification.

This review addressed

the impact of: performing the modification during the refueling

outage with fuel in the vessel, on routine operation, on the high energy line break study,

on pump available net positive suction head, on hydraulic design considerations,

on the

seismic interaction evaluation, on consistency with Regulatory Guide 1.82, "Sumps for

Emergency Core Cooling and Containment Spray Systems," material compatibility and

consistency with licensing documents,

in addition to other design considerations.

The 10 CFR 50.59 safety evaluation concluded that an unreviewed safety question

was'ot

involved, nor was a change to the Technical Specifications involved. The proposed

Final Safety Analysis Report Update change and revision to Design Criteria

Memorandum T-16, "Containment Function," were consistent with the modification. The

design change package was prepared

in accordance with the applicable

Procedure, CF33.ID9, "Design Change Package Development." The inspectors

identified no concerns with these reviews.

Following the completion of modification, the sump was inspected for openings in the

structure or potential flow paths that could bypass the screens.

No openings greater

than that specified in the design were found. Potential openings around piping or

supports that penetrated the sump structure were effectively closed.

Joints between

sections of grating and between the edges of the screen and the supporting structure

were effective closed by the design and installation of the modification.

c.

Conclusions

, The inspectors concluded that the design change package and associated

safety

evaluation for replacement of the Unit 2 recirculation sump screens was comprehensive,

and the conclusions were reasonable.

The design change was effective in improving

the containment sump's ability to screen out debris that could block safety injection flow

paths.

~ t

-28-

ES

Miscellaneous Engineering Issues (92901)

E8.1

Closed

Violation 96016-06

failure to perform prompt operability assessment.

The

inspectors identified that following documentation of degraded conditions in the diesel

generator voltage regulator boards, the licensee failed to perform a prompt operability

assessment.

For corrective actions, the licensee:

(1) replaced the voltage regulator

boards, (2) established

a daily action request review team that screens each new action

request for operability issues, (3) trained nuclear technical services personnel in the

license procedures for operability assessments,

(4) revised Procedure OM7.ID12

"Prompt Operability Assessments"

to'require shift supervisor notification of all degraded

conditions, (5) briefed all shift supervisors on the responsibility for maintaining

operability, (6) issued an all employee letter emphasizing management expectations

with respect to operability assessments,

(7) initiated an engineering directors meeting to

discuss emergent issues that may have operability concerns, and (8) performed a case

study on lessons learned from the violation. The inspectors reviewed documentation

that established that these items have been completed satisfactorily. This item is

closed.

.P

R1

Radiological Protection and Chemistry Controls

R1.1

General Comments

During this inspection period, the inspectors observed radiation protection controls.

The

inspectors noted that licensee personnel followed basic radiation practices such as

proper wearing of dosimetry and observance of radiation protection boundaries.

Licensee management's

efforts to keep exposures as low as reasonably achievable

during Refueling Outage 2R8 appeared to be successful in that total outage exposure

was 147 person-rem, while the outage exposure goal was 160 person-rem. The

licensee's cleanup of the reactor coolant system following shutdown of Unit 2, and the

use of mock-up training for several outage tasks, contributed to the lower exposure.

This was an improvement over previous refueling outages.

S1

Conduct of Security and Safeguards Activities

S1.1

General Comments

71750

During routine tours, the inspectors noted that the security officers were alert at their

posts, security boundaries were being maintained properly, and screening processes

at

the Primary Access Point were performed well. During backshift inspections, the

inspectors noted that the protected area was properly illuminated, especially in areas

where temporary equipment was brought in.

0

-29-

V. Mana ement Meetin s

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management at the

conclusion of the inspection on April7, 1998. The licensee acknowledged the findings

presented.

The inspectors asked the licensee whether any materials examined during the inspection

should be considered proprietary.

No proprietary information was identified.

t

0

TT CHMENT

SUPPLEMENT

L INFORMATIO

PARTIALLIST OF PERSONS CONTACTED

Licensee

W. G. Crockett, Manager, Nuclear Quality Services

R. D. Gray, Director, Radiation Protection

T. L. Grebel, Director, Regulatory Services

S. A. Hiett, Director, Operations

D. B. Miklush, Manager, Engineering Services

J. E. Molden, Manager, Operations

Services'.

H. Oatley, Manager, Maintenance Servi'ces

R. P. Powers, Vice President and Plant Manager

L. F. Womack, Vice President, Nuclear Technical Services

INSPECTION PROCEDURES (IP) USED

IP 37551

IP 60710

IP 61726

IP 62707

IP 71707

IP 71750

IP 92902

IP 92903

IP 93702

Onsite Engineering

Refueling Activities

Surveillance Observations

Maintenance Observation

Plant Operations

Plant Support Activities

Followup - Maintenance

Followup - Engineering

Prompt Onsite Response to Events at Operating Power Reactors

/s

0

-2-

0~coed

ITEMS OPENED AND CLOSED

50-323/

98007-02

50-323/

98007-03

50-275;323/

98007-04

50-275;323/

98007-05

C~los

d

VIO

VIO

VIO

VIO

Failure to provide appropriate procedure for nonseismic

hoist stowage (Section 01.3)

Failure to restore high flux alarm during core reload

(Section 01.5)

Multiple failures to implement clearance procedure

(Section 01.6)

Failure to implement design of level indicating system into

abnormal procedures (Section 03.1)

50-275;323/

96016-06

VIO

Failure to perform prompt operability assessment

(Section E8.1)

ened and Closed

50-275;323/

98007-01

NCV

Failure to provide an appropriate procedure for switching

power supplies (Section 01.2)

50-27;323/

98007-06

NCV

Inadequate ground buggy installation procedure

(Section M4.1)

.

Discussed

50-275;323/

96014-03

VIO

Failure to remove action request tags from the control

boards (Section M8.1).

(

e

0

'I