IR 05000397/2012003

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IR 05000397-12-003; 03/24/2012 - 06/22/2012; Columbia Generating Station, Integrated Resident and Regional Report; Operability Evaluations and Functionality Assessments; Post-Maintenance Testing; Surveillance Testing
ML12206A565
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 07/24/2012
From: Webb Patricia Walker
NRC/RGN-IV/DRP/RPB-A
To: Reddemann M
Energy Northwest
Walker W
References
IR-12-003
Download: ML12206A565 (60)


Text

UNITED STATES uly 24, 2012

SUBJECT:

COLUMBIA GENERATING STATION - NRC INTEGRATED INSPECTION REPORT 05000397/2012003

Dear Mr. Reddemann:

On June 22, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Columbia Generating Station. The enclosed inspection report documents the inspection results which were discussed on July 2, 2012, with Mr. W. Hettel, Vice President, Operations and other members of your staff.

The inspections examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

Three NRC identified findings of very low safety significance (Green) were identified during this inspection. All of these findings were determined to involve violations of NRC requirements.

Further, two licensee-identified violations which were determined to be of very low safety significance are listed in this report. The NRC is treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest these non-cited violations, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Columbia Generating Station.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region IV; and the NRC Resident Inspector at Columbia Generating Station.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's Agencywide Document Access and Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Wayne Walker, Chief Project Branch A Division of Reactor Projects Docket No: 05000397 License No: NPF-21 Enclosure: NRC Inspection Report 05000397/2012003 w/ Attachment: Supplemental Information cc w/ encl: Electronic Distribution

SUMMARY OF FINDINGS

IR 05000397/2012003; 03/24/2012 - 06/22/2012; Columbia Generating Station, Integrated

Resident and Regional Report; Operability Evaluations and Functionality Assessments;

Post-Maintenance Testing; Surveillance Testing.

The report covered a 3-month period of inspection by resident inspectors and announced baseline inspections by region-based inspectors. Three Green non-cited violations of significance were identified. The significance of most findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual Chapter 0609, Significance Determination Process. The cross-cutting aspect is determined using Inspection Manual Chapter 0310, Components Within the Cross Cutting Areas. Findings for which the significance determination process does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,

Revision 4, dated December 2006.

NRC-Identified Findings and Self-Revealing Findings

Cornerstone: Mitigating Systems

Green.

The inspectors identified a non-cited violation of 10 CFR Part 50, Appendix B,

Criterion V, Instructions, Procedures and Drawings, for the failure of the licensee to perform a required operability determination for a degraded condition associated with residual heat removal pump B. On March 25, 2012, the licensee performed Procedure OSP-RHR/IST-Q703, RHR Loop B Operability Test, Revision 34, and recorded a pump discharge pressure that exceeded the acceptance criteria by 0.03 psig. The operating crew determined that no immediate operability determination was required by Procedure PPM 1.3.66, Operability and Functionality Evaluation," Revision 20, since pump performance was stable and satisfactory. Subsequent review by the inspectors revealed that the assumption that pump performance was stable and satisfactory was not correct and an operability determination was required.

Specifically, pump discharge pressure dropped below the technical specification surveillance requirement acceptance criteria at several points after the licensee had recorded their data and the pump had exhibited a declining trend in performance since its last surveillance. This issue was entered into the licensees corrective action program as Action Request AR 266371.

This performance deficiency was more than minor because it affected the equipment performance attribute of the Mitigating Systems Cornerstone objective of ensuring the reliability of systems that respond to initiating events. The inspectors performed an initial screening of the finding in accordance with IMC 0609.04, Phase 1 - Initial Screening and Characterization of Findings. The inspectors determined this finding to be of very low safety significance (Green) because it did not result in the loss of a system safety function, did not represent the loss of safety function of a single train for greater than its allowed outage time, did not result in the loss of safety function of any non-technical specification equipment, and did not screen as potentially risk significant due to seismic, flooding, or severe weather initiating events. The inspectors determined that this finding had a cross-cutting aspect in the area of human performance associated with the decision making component because the licensee failed to use conservative assumptions when evaluating Action Request AR 260478 that documented low margin for residual heat removal pump B. Specifically, the shift manager failed to challenge the non-conservative assumption that pump flow was stable and satisfactory H.1(b). (Section 1R15).

Green.

The inspectors identified a non-cited violation of 10 CFR Part 50, Appendix B,

Criterion XI, Test Control, for the failure of the licensee to perform a required postmaintenance test of the division 3 safety-related batteries prior to system restoration. On May 22, 2012, the licensee replaced the division 3 safety-related battery HPCS-B1-DG3 under Work Order 02000618. The resident inspectors reviewed the work orders associated with the replacement of battery HPCS-B1-DG3 and identified that the licensee failed to incorporate either a modified performance discharge test or a battery service test into their postmaintenance testing for battery HPCS-B1-DG3 and restored the equipment to operable without meeting Technical Specification Surveillance Requirement 3.8.4.3. Following identification, the licensee performed a battery service test and determined that the division 3 battery capacity was adequate to meet all operability requirements. The licensee initiated corrective action documents Action Requests AR 264204 and AR 264214 to address the failure to include all technical specification requirements into postmaintenance testing for battery HPCS-B1-DG3.

This performance deficiency was more than minor because it affected the configuration control attribute of the Mitigating Systems Cornerstone objective of ensuring the reliability of systems that respond to initiating events. The inspectors performed an initial screening of the finding in accordance with IMC 0609.04, Phase 1 - Initial Screening and Characterization of Findings. The inspectors determined this finding to be of very low safety significance (Green) because the finding was a qualification deficiency confirmed not to result in loss of operability. The inspectors determined that this finding had a cross-cutting aspect in the area of human performance associated with the decision making component because the licensee failed to obtain an interdisciplinary review on the postmaintenance testing planned for battery HPCS-B1-DG3. Specifically, the shift manager failed to request input from system engineering and licensing on the decision to not perform a battery service test

H.1(a). (Section 1R19).

Green.

The inspectors identified a non-cited violation of 10 CFR Part 50, Appendix B,

Criterion V, Instructions, Procedures and Drawings, for the failure of the licensee to control impairment of high energy line break barriers in accordance with Procedure PPM 1.3.57, Barrier Impairment," Revision 28. On May 6, 2012, the licensee performed Surveillance Procedure ISP-CIA-Q901, ADS Accumulator Backup Low Pressure Alarm Division 1 CFT/CC," Revision 7. A high energy line break barrier associated with instrument rack E-IR-67 was breached and left unattended during the surveillance. The licensee failed to meet requirements specified in Procedure PPM 1.3.57, Barrier Impairment," Revision 28, which required a barrier impairment permit for the high energy line break barrier that was breached. Additionally, the inspectors determined that the licensee failed to declare inoperable and unavailable, all equipment impacted by the breached high energy line break barrier on instrument rack E-IR-67. As interim corrective action, the licensee initiated Night Order 1379 directing a more complete review of Procedure PPM 1.3.57 prior to work authorization on components that serve as hazard barriers. This issue was entered into the licensees corrective action program as Action Request AR 263274.

This performance deficiency was more than minor because it affected the configuration control attribute of the Mitigating Systems Cornerstone objective of ensuring the availability of systems that respond to initiating events. The inspectors performed an initial screening of the finding in accordance with IMC 0609.04,

"Phase 1 - Initial Screening and Characterization of Findings." The inspectors determined this finding to be of very low safety significance (Green) because it did not result in the loss of a system safety function, did not represent the loss of safety function of a single train for greater than its allowed outage time, did not result in the loss of safety function of any non-technical specification equipment, and did not screen as potentially risk significant due to seismic, flooding, or severe weather initiating events. The inspectors determined that this finding had a cross-cutting aspect in the area of human performance associated with the resources component because the licensee failed to update surveillance procedures associated with high energy line break barriers such that individuals responsible for maintaining those barriers were knowledgeable of the requirements in Procedure PPM 1.3.57 H.2(c).

(Section 1R22).

Licensee-Identified Violations

Violations of very low safety significance that were identified by the licensee have been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. These violations and associated corrective action tracking numbers are listed in Section 4OA7 of this report.

REPORT DETAILS

Summary of Plant Status

The plant began the inspection period at 100 percent power. Periodically between March 30, 2012 and May 19, 2012, the station reduced power to 85 percent at the request of the local grid operator for economic dispatch. On May 19, 2012, the station shut down for a planned maintenance outage. On May 29, 2012 the station exited the maintenance outage and reached 100% power on May 31, 2012. The facility operated at 100 percent power, with the exception of scheduled reductions in power to support minor maintenance and testing, and requested economic dispatch for the remainder of the inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

Summer Readiness for Offsite and Alternate-ac Power

a. Inspection Scope

The inspectors performed a review of preparations for summer weather for selected systems, including conditions that could lead to loss-of-offsite power and conditions that could result from high temperatures. The inspectors reviewed the procedures affecting these areas and the communications protocols between the transmission system operator and the plant to verify that the appropriate information was being exchanged when issues arose that could affect the offsite power system. Examples of aspects considered in the inspectors review included:

  • The coordination between the transmission system operator and the plants operations personnel during off-normal or emergency events
  • The explanations for the events
  • The estimates of when the offsite power system would be returned to a normal state
  • The notifications from the transmission system operator to the plant when the offsite power system was returned to normal During the inspection, the inspectors focused on plant-specific design features and the procedures used by plant personnel to mitigate or respond to adverse weather conditions. Additionally, the inspectors reviewed the FSAR and performance requirements for systems selected for inspection, and verified that operator actions were appropriate as specified by plant-specific procedures. Specific documents reviewed during this inspection are listed in the attachment. The inspectors also reviewed corrective action program items to verify that the licensee was identifying adverse weather issues at an appropriate threshold and entering them into their corrective action program in accordance with station corrective action procedures. The inspectors reviews focused specifically on the following plant systems:
  • Plant Switchyard (Ashe Substation) and Transformer Yard

b. Findings

No findings were identified.

1R04 Equipment Alignment

.1 Partial Walkdown

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant systems:

  • May 24, 2012, control rod drive system in preparation for reactor startup following maintenance outage
  • June 18, 2012, divisions 1, 2, and 3; 125 Vdc and 250 Vdc electrical systems The inspectors selected these systems based on their risk significance relative to the reactor safety cornerstones at the time they were inspected. The inspectors attempted to identify any discrepancies that could affect the function of the system, and, therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, system diagrams, FSAR, technical specification requirements, administrative technical specifications, outstanding work orders, condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems incapable of performing their intended functions. The inspectors also inspected accessible portions of the systems to verify system components and support equipment were aligned correctly and operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies. The inspectors also verified that the licensee had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the corrective action program with the appropriate significance characterization. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of four partial system walkdown samples as defined in Inspection Procedure 71111.04-05.

b. Findings

No findings were identified.

.2 Complete Walkdown

a. Inspection Scope

On May 1, 2012, the inspectors performed a complete system alignment inspection of the containment instrument air system including the safety-related nitrogen supply to the automatic depressurization system to verify the functional capability of the system. The inspectors selected this system because it was considered both safety significant and risk significant in the licensees probabilistic risk assessment. The inspectors inspected the system to review mechanical and electrical equipment lineups, electrical power availability, system pressure and temperature indications, as appropriate, component labeling, component lubrication, component and equipment cooling, hangers and supports, operability of support systems, and to ensure that ancillary equipment or debris did not interfere with equipment operation. The inspectors reviewed a sample of past and outstanding work orders to determine whether any deficiencies significantly affected the system function. In addition, the inspectors reviewed the corrective action program database to ensure that system equipment alignment problems were being identified and appropriately resolved. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one complete system walkdown sample as defined in Inspection Procedure 71111.04-05.

b. Findings

No findings were identified.

1R05 Fire Protection

.1 Quarterly Fire Inspection Tours

a. Inspection Scope

The inspectors conducted fire protection walkdowns that were focused on availability, accessibility, and the condition of firefighting equipment in the following risk-significant plant areas:

  • April 11, 2012, Fire Areas SW-1 and SW-2, service water pump houses A and B
  • April 17, 2012, Fire Area R-1, reactor building 606 elevation
  • April 23, 2012, fire areas associated with barrier impairments issued for extended allowed outage time for diesel generator 2 being out of service
  • June 8, 2012, Main Control Room The inspectors reviewed areas to assess if licensee personnel had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant; effectively maintained fire detection and suppression capability; maintained passive fire protection features in good material condition; and had implemented adequate compensatory measures for out of service, degraded or inoperable fire protection equipment, systems, or features, in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plants Individual Plant Examination of External Events with later additional insights, their potential to affect equipment that could initiate or mitigate a plant transient, or their impact on the plants ability to respond to a security event. Using the documents listed in the attachment, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed; that transient material loading was within the analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition. The inspectors also verified that minor issues identified during the inspection were entered into the licensees corrective action program.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of four quarterly fire-protection inspection samples as defined in Inspection Procedure 71111.05-05.

b. Findings

No findings were identified.

1R06 Flood Protection Measures

a. Inspection Scope

The inspectors reviewed the FSAR, the flooding analysis, and plant procedures to assess susceptibilities involving internal flooding; reviewed the corrective action program to determine if licensee personnel identified and corrected flooding problems; inspected underground bunkers/manholes to verify the adequacy of sump pumps, level alarm circuits, cable splices subject to submergence, and drainage for bunkers/manholes; and verified that operator actions for coping with flooding can reasonably achieve the desired outcomes. The inspectors also inspected the areas listed below to verify the adequacy of equipment seals located below the flood line, floor and wall penetration seals, watertight door seals, common drain lines and sumps, sump pumps, level alarms, and control circuits, and temporary or removable flood barriers. Specific documents reviewed during this inspection are listed in the attachment.

  • April 3, 2012, manholes 8 and 9 These activities constitute completion of one bunker/manhole sample as defined in Inspection Procedure 71111.06-05.

b. Findings

No findings were identified.

1R07 Heat Sink Performance

a. Inspection Scope

The inspectors reviewed licensee programs, verified performance against industry standards, and reviewed critical operating parameters and maintenance records for the residual heat removal 1A heat exchanger. The inspectors verified that performance tests were satisfactorily conducted for heat exchangers/heat sinks and reviewed for problems or errors; the licensee utilized the periodic maintenance method outlined in EPRI Report NP 7552, Heat Exchanger Performance Monitoring Guidelines; the licensee properly utilized biofouling controls; the licensees heat exchanger inspections adequately assessed the state of cleanliness of their tubes; and the heat exchanger was correctly categorized under 10 CFR 50.65, Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one heat sink inspection sample as defined in Inspection Procedure 71111.07-05.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program and Licensed Operator Performance

.1 Quarterly Review of Licensed Operator Requalification Program

a. Inspection Scope

On May 30, 2012, the inspectors observed a crew of licensed operators in the plants simulator during requalification testing. The inspectors assessed the following areas:

  • Licensed operator performance
  • The ability of the licensee to administer the evaluations
  • The modeling and performance of the control room simulator
  • The quality of post-scenario critiques
  • Follow-up actions taken by the licensee for identified discrepancies These activities constitute completion of one quarterly licensed operator requalification program sample as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

.2 Quarterly Observation of Licensed Operator Performance

a. Inspection Scope

The inspectors observed the operators performance of the following activities:

  • April 25, 2012, replacement of a failed digital electro-hydraulic power supply that had the potential to create a plant transient if performed incorrectly.
  • April 30, 2012, reduction of reactor power to 85 percent at the request of the local grid operator.
  • May 28, 2012, plant startup activities in the main control room following completion of Maintenance Outage 12-01.

In addition, the inspectors assessed the operators adherence to plant procedures, including OI-9, "Operations Standards and Expectations," and other operations department policies.

These activities constitute completion of one quarterly licensed-operator performance sample as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following risk significant systems:

  • April 24, 2012, diesel generator 4; alternate AC diesel generator
  • June 21, 2012, division 1, 2, and 3; 125 Vdc and 250 Vdc distribution system The inspectors reviewed events such as where ineffective equipment maintenance has resulted in valid or invalid automatic actuations of engineered safeguards systems and independently verified the licensee's actions to address system performance or condition problems in terms of the following:
  • Implementing appropriate work practices
  • Identifying and addressing common cause failures
  • Characterizing system reliability issues for performance
  • Charging unavailability for performance
  • Trending key parameters for condition monitoring
  • Verifying appropriate performance criteria for structures, systems, and components classified as having an adequate demonstration of performance through preventive maintenance, as described in 10 CFR 50.65(a)(2), or as requiring the establishment of appropriate and adequate goals and corrective actions for systems classified as not having adequate performance, as described in 10 CFR 50.65(a)(1)

The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system. In addition, the inspectors verified maintenance effectiveness issues were entered into the corrective action program with the appropriate significance characterization. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of two quarterly maintenance effectiveness samples as defined in Inspection Procedure 71111.12-05.

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed licensee personnel's evaluation and management of plant risk for the maintenance and emergent work activities affecting risk-significant and safety-related equipment listed below to verify that the appropriate risk assessments were performed prior to removing equipment for work:

  • April 9, 2012, performing division 1 scheduled work during emergent entry into division 2 residual heat removal technical specification action statement
  • April 16, 2012, unplanned Yellow risk due to emergent issue with fuel pool cooling pump 1A
  • May 22, 2012, planned Yellow risk during work on backup transformer TR-B
  • May 31, 2012, planned Yellow risk during standby liquid control train B maintenance outage and unexpected loss of reactor protection system bus B The inspectors selected these activities based on potential risk significance relative to the reactor safety cornerstones. As applicable for each activity, the inspectors verified that licensee personnel performed risk assessments as required by 10 CFR 50.65(a)(4)and that the assessments were accurate and complete. When licensee personnel performed emergent work, the inspectors verified that the licensee personnel promptly assessed and managed plant risk. The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensee's probabilistic risk analyst or shift technical advisor, and verified plant conditions were consistent with the risk assessment. The inspectors also reviewed the technical specification requirements and inspected portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of four maintenance risk assessments and emergent work control inspection samples as defined in Inspection Procedure 71111.13-05.

b. Findings

No findings were identified.

1R15 Operability Evaluations and Functionality Assessments

a. Inspection Scope

The inspectors reviewed the following assessments:

  • May 3, 2012, Action Request AR 262795 documenting a potential concern with diesel generator 2 consuming more fuel while operating
  • May 23, 2012, Action Request AR 263887 documenting containment vacuum breaker CVB-V-1JK rear disc found open The inspectors selected these operability and functionality assessments based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the evaluations to ensure technical specification operability was properly justified and to verify the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the technical specifications and FSAR to the licensees evaluations to determine whether the components or systems were operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. Additionally, the inspectors reviewed a sampling of corrective action documents to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of four operability evaluations inspection samples as defined in Inspection Procedure 71111.15-05.

b. Findings

Introduction.

The inspectors identified a Green non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures and Drawings, for the licensees failure to perform a required operability determination for a degraded condition associated with residual heat removal pump B.

Description.

On March 25, 2012, the licensee performed Procedure OSP-RHR/IST-Q703, RHR Loop B Operability Test," Revision 34. Step 7.2.68 of the procedure was used to demonstrate the residual heat removal pumps ability to provide greater than 7,450 gallons per minute with a differential pressure of greater than or equal to 26 psid between the reactor vessel and the pumps suction source. This procedural step was provided to satisfy the requirements of Technical Specification Surveillance Requirement 3.5.1.4. Due to the design of the system, the surveillance was performed by establishing a pump flow to the suppression pool that exceeded the surveillance requirement limit then measured pump discharge pressure as a means of demonstrating that the system was capable of overcoming the required differential pressure and system losses. During performance of Step 7.2.68, the licensee recorded a pump discharge pressure that exceeded the acceptance criteria by 0.03 psig. The operating crew reviewed the results of the surveillance and noted the low margin to the technical specification requirement but declared the surveillance met and the equipment operable based on the 0.03 psig of margin. No formal evaluation of the low margin was performed.

On March 28, 2012, the inservice testing engineer initiated Action Request AR 00260478 to document the residual heat removal pumps low margin to Technical Specification Surveillance Requirement 3.5.1.4. The action request initiator noted that pump performance was stable and satisfactory. The shift manager who performed the operations review of Action Request AR 00260478 determined that no operability determination was required by Procedure PPM 1.3.66, Operability and Functionality Evaluation," Revision 20 because the pump had passed its most recent surveillance.

When determining the need for an operability determination, the shift manager did not consider the required mission time for residual heat removal pump B or if pump performance was degrading such that the reasonable expectation of operability would be lost prior to the next scheduled performance of Procedure OSP-RHR/IST-Q703.

On April 5, 2012, the inspectors reviewed Action Request AR 260478 and the March 25, 2012, performance of Procedure OSP-RHR/IST-Q703. Plant computer data revealed that the residual heat removal pump did meet the procedure acceptance criteria at the moment the data was recorded; however, pump discharge pressure dropped below the technical specification surveillance requirement acceptance criteria at several points after the licensee had recorded their data. Additionally, comparison of previous performance of Procedure OSP-RHR/IST-Q703 revealed a declining trend in pump discharge pressure. Specifically, pump discharge pressure dropped from 1.75 psig above the technical specification acceptance criteria on January 2, 2012, to only 0.03 psig on March 25, 2012. This data suggested that the licensees conclusion that performance was stable and satisfactory, as documented in Action Request AR 260478, was incorrect. A significant drop in pump discharge pressure, such that the reasonable expectation of operability would be lost prior to the next scheduled performance of the surveillance, was a degraded condition. Procedure PPM 1.3.66, Step 4.1.6, requires the licensee to immediately determine operability from a detailed examination of the deficiency. The inspectors determined that the licensee failed to evaluate for operability Action Request AR 260478. Because the licensee failed to perform an immediate operability determination, they also failed to recognize that the residual heat removal pump B was inoperable following the March 25, 2012, performance of Procedure OSP-RHR/IST-Q703.

Upon notification of the degraded condition, the shift manager requested assistance from engineering who confirmed that the residual heat removal pump B failed to meet Technical Specification Surveillance Requirement 3.5.1.4 during the performance of Procedure OSP-RHR/IST-Q703 on March 25, 2012. The pump was declared inoperable and Technical Specification Limiting Condition for Operation 3.5.1 Condition A was entered which required the equipment to be restored within 7 days. On April 6-9, 2012, the licensee performed additional testing of residual heat removal pump B which confirmed that the pump was unable to meet Technical Specification Surveillance Requirement 3.5.1.4. As interim corrective actions, the licensee re-modeled the flow path used in the residual heat removal system to include both the heat exchanger and heat exchanger bypass lines. By adding this additional flow path, the licensee removed conservatisms incorporated into the surveillance requirement acceptance criteria by reducing the pressure drop across the system. This allowed the licensee to reduce the required pump discharge pressure specified in Procedure OSP-RHR/IST-Q703 and exit Technical Specification Limiting Condition for Operation 3.5.1 Condition A. Long term corrective actions are planned by the licensee to request a technical specifications amendment to reduce the required residual heat removal pump flow such that the flows more closely align with the assumptions of the accident analysis.

Analysis.

The failure to perform an immediate determination of operability for a degraded condition in accordance with Procedure PPM 1.3.66 was a performance deficiency. This performance deficiency was more than minor because it affected the equipment performance attribute of the Mitigating Systems Cornerstone objective of ensuring the reliability of systems that respond to initiating events. The inspectors performed an initial screening of the finding in accordance with IMC 0609.04, "Phase 1 - Initial Screening and Characterization of Findings." The inspectors determined this finding to be of very low safety significance (Green) because it did not result in the loss of a system safety function, did not represent the loss of safety function of a single train for greater than its allowed outage time, did not result in the loss of safety function of any non-technical specification equipment, and did not screen as potentially risk significant due to seismic, flooding, or severe weather initiating events.

The inspectors determined that this finding had a cross-cutting aspect in the area of human performance associated with the decision making component because the licensee failed to use conservative assumptions when evaluating Action Request AR 260478 that documented low margin for residual heat removal pump B. Specifically, the shift manager failed to challenge the non-conservative assumption that pump flow was stable and satisfactory H.1(b).

Enforcement.

Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures and Drawings," requires, in part, that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings. Licensee Procedure PPM 1.3.66, Operability and Functionality Evaluation," Revision 20, Step 4.1.6, required the licensee to immediately determine operability from a detailed examination of the deficiency. Operability should be determined immediately upon discovery that structures, systems and components subject to technical specifications are in a degraded or nonconforming condition.

Contrary to the above, on March 28, 2012, the licensee failed to evaluate for operability Action Request AR 260478 which documented a significant drop in residual heat removal pump B performance and low margin to Technical Specification Surveillance Requirement 3.5.1.4. Consequently, the licensee failed to recognize that the residual heat removal pump B was inoperable following the March 25, 2012, performance of Procedure OSP-RHR/IST-Q703. The licensee implemented corrective actions to modify the testing procedure by removing conservatisms associated with the assumed residual heat removal flow path. Because this violation was of very low safety significance (Green) and it was entered into the licensees corrective action program as Action Request AR 266371, this violation is being treated as a non-cited violation, consistent with the Enforcement Policy: NCV 05000397/2012003-01, Failure to Evaluate Operability Associated with Residual Heat Removal Pump B.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed the following post-maintenance activities to verify that procedures and test activities were adequate to ensure system operability and functional capability:

  • April 25, 2012, postmaintenance testing of diesel generator 2 upon completion of planned maintenance activities
  • May 27, 2012, postmaintenance testing of division 3 safety-related batteries following planned replacement
  • June 1, 2012, postmaintenance testing of reactor recirculation pump 1A following planned replacement of upper seal package The inspectors selected these activities based upon the structure, system, or component's ability to affect risk. The inspectors evaluated these activities for the following:
  • The effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed
  • Acceptance criteria were clear and demonstrated operational readiness; test instrumentation was appropriate The inspectors evaluated the activities against the technical specifications, the FSAR, 10 CFR Part 50 requirements, licensee procedures, and various NRC generic communications to ensure that the test results adequately ensured that the equipment met the licensing basis and design requirements. In addition, the inspectors reviewed corrective action documents associated with post-maintenance tests to determine whether the licensee was identifying problems and entering them in the corrective action program and that the problems were being corrected commensurate with their importance to safety. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of four post-maintenance testing inspection samples as defined in Inspection Procedure 71111.19-05.

b. Findings

Introduction.

The inspectors identified a Green non-cited violation of 10 CFR Part 50, Appendix B, Criterion XI, Test Control, for the failure of the licensee to perform a required postmaintenance test of the division 3 safety-related batteries prior to system restoration.

Description.

On May 22, 2012, during a planned maintenance outage, the licensee replaced the division 3 safety-related battery HPCS-B1-DG3 under Work Order 02000618. Prior to installation, the licensee performed acceptance testing in accordance with Procedure ESP-BSPARE-A101, 12 Month Spare Battery Cell Inspection," Revision 2. This procedure provided two options for testing; either a performance discharge test or a modified performance discharge test. For the work performed under Work Order 02000618, the licensee elected to perform the performance discharge test. On May 24, 2012, operations logged that battery HPCS-B1-DG3 was operable following completion of replacement activities under Work Order 02000618.

On May 25, 2012, the resident inspectors reviewed the work orders associated with the replacement of battery HPCS-B1-DG3. Operability testing requirements of safety-related battery are specified in Limiting Condition for Operation (LCO) 3.8.4, DC Sources - Operating and LCO 3.8.6, Battery Parameters. Technical Specification Surveillance Requirement 3.8.4.3 requires a battery service test to verify battery capacity is adequate to supply the required emergency loads for the design duty cycle.

Surveillance Requirement 3.8.4.3 is modified by a note that allows the licensee to perform the modified performance discharge test in Surveillance Requirement 3.8.6.6 in lieu of the service test in Surveillance Requirement 3.8.4.3. The modified performance discharge is different from the performance discharge test in that it verifies the ability of the battery to provide a high rate, short duration load to meet the critical period of the load duty cycle. Since no battery service test was performed and the licensee elected to perform a performance discharge test instead of a modified performance discharge test, the inspectors concluded that the licensee restored battery HPCS-B1-DG3 to operable without meeting Technical Specification Surveillance Requirement 3.8.4.3.

Following identification that not all technical specification requirements were incorporated into the postmaintenance testing for battery HPCS-B1-DG3, the licensee initiated Work Order 02026256 to perform battery service testing under Procedure ESP-B1DG3-B101, 24 Month Battery Testing of 125 VDC HPCS-B1-DG3, Revision 17.

Testing was performed on May 25, 2012, and determined that the division 3 battery capacity was adequate to meet all operability requirements. The licensee initiated corrective action documents Action Requests AR 264204 and AR 264214 to address the failure to include all technical specification requirements into postmaintenance testing for battery HPCS-B1-DG3.

The inspectors determined that Work Order 02000618 was originally planned to incorporate a battery service test as specified in Procedure ESP-B1DG3-B101 but was later changed to credit the acceptance testing performed in ESP-BSPARE-A101 in lieu of a battery service test. Neither system engineering or licensing was contacted by operations staff for determination of technical specification impacts of not performing Procedure ESP-B1DG3-B101.

Analysis.

The failure to perform adequate postmaintenance testing of the division 3 electrical batteries was a performance deficiency. This performance deficiency was more than minor because it affected the configuration control attribute of the Mitigating Systems Cornerstone objective of ensuring the reliability of systems that respond to initiating events. The inspectors performed an initial screening of the finding in accordance with IMC 0609.04, "Phase 1 - Initial Screening and Characterization of Findings." The inspectors determined this finding to be of very low safety significance (Green) because the finding was a qualification deficiency confirmed not to result in loss of operability. The inspectors determined that this finding had a cross-cutting aspect in the area of human performance associated with the decision making component because the licensee failed to obtain an interdisciplinary review on the postmaintenance testing planned for battery HPCS-B1-DG3. Specifically, the shift manager failed to request input from system engineering and licensing on the decision to not perform a battery service test H.1(a).

Enforcement.

Title 10 CFR Part 50, Appendix B, Criterion XI, Test Control," requires, in part, that a test program shall be established to assure that all testing required to demonstrate that structures, systems, and components will perform satisfactorily in service is identified and performed in accordance with written test procedures. The test program shall include, as appropriate, preoperational tests, and operational tests.

Contrary to the above, on May 24, 2012, the licensee restored safety-related battery HPCS-B1-DG3 to service without performing an adequate preoperational test to demonstrate that the battery would perform satisfactorily in service. Specifically, the licensee failed to include either a modified performance discharge test or a battery service test into their postmaintenance testing for battery HPCS-B1-DG3. Because this violation was of very low safety significance (Green) and it was entered into the licensees corrective action program as Action Requests AR 264204 and AR 264214, this violation is being treated as a non-cited violation, consistent with the Enforcement Policy: NCV 05000397/2012003-02, Failure to Establish Adequate Postmaintenance Tests for Replacement of Division 3 Safety Related Batteries.

1R20 Refueling and Other Outage Activities

a. Inspection Scope

The inspectors reviewed the outage safety plan and contingency plans for Maintenance Outage 12-01, conducted May 23-29, 2012, to confirm that licensee personnel had appropriately considered risk, industry experience, and previous site-specific problems in developing and implementing a plan that assured maintenance of defense in depth.

During the maintenance outage, the inspectors monitored licensee controls over the outage activities listed below:

  • Configuration management, including maintenance of defense in depth, is commensurate with the outage safety plan for key safety functions and compliance with the applicable technical specifications when taking equipment out of service
  • Clearance activities, including confirmation that tags were properly hung and equipment appropriately configured to safely support the work or testing
  • Installation and configuration of reactor coolant pressure, level, and temperature instruments to provide accurate indication, accounting for instrument error
  • Status and configuration of electrical systems to ensure that technical specifications and outage safety-plan requirements were met, and controls over switchyard activities
  • Verification that outage work was not impacting the ability of the operators to operate the spent fuel pool cooling system
  • Reactor water inventory controls, including flow paths, configurations, and alternative means for inventory addition, and controls to prevent inventory loss
  • Controls over various activities that could affect reactivity
  • Startup and ascension to full power operation, tracking of startup prerequisites, walkdown of the drywell (primary containment) to verify that debris had not been left which could block emergency core cooling system suction strainers, and reactor physics testing
  • Licensee identification and resolution of problems related to refueling outage activities Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one refueling outage and other outage inspection sample as defined in Inspection Procedure 71111.20-05.

b. Findings

No findings were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors reviewed the FSAR, procedure requirements, and technical specifications to ensure that the surveillance activities listed below demonstrated that the systems, structures, and/or components tested were capable of performing their intended safety functions. The inspectors either witnessed or reviewed test data to verify that the significant surveillance test attributes were adequate to address the following:

  • Preconditioning
  • Evaluation of testing impact on the plant
  • Acceptance criteria
  • Test equipment
  • Procedures
  • Test data
  • Testing frequency and method demonstrated technical specification operability
  • Restoration of plant systems
  • Fulfillment of ASME Code requirements
  • Updating of performance indicator data
  • Engineering evaluations, root causes, and bases for returning tested systems, structures, and components not meeting the test acceptance criteria were correct
  • Reference setting data
  • Annunciators and alarms setpoints The inspectors also verified that licensee personnel identified and implemented any needed corrective actions associated with the surveillance testing.
  • April 8, 2012, OSP-RHR/IST-Q703, RHR Loop B Operability Test," Revision 34
  • April 12, 2012, OSP-ELEC-M701, Diesel Generator 1 - Monthly Operability Test," Revision 49
  • April 19, 2012, OSP-ELEC-S703, HPCS Diesel Generator Semi-Annual Operability Test, Revision 51

Revision 8 (Determination of cooldown rate to meet SR 3.4.11.1)

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of five surveillance testing inspection samples as defined in Inspection Procedure 71111.22-05.

b. Findings

Introduction.

The inspectors identified a Green non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures and Drawings, for the licensees failure to control impairment of high energy line break barriers in accordance with Procedure PPM 1.3.57, Barrier Impairment," Revision 28.

Description.

On May 6, 2012, the licensee performed Surveillance Procedure ISP-CIA-Q901, ADS Accumulator Backup Low Pressure Alarm Division 1 CFT/CC,"

Revision 7, to test the alarm and safety-related isolation function of the instrument air supply to the automatic depressurization system. As part of the surveillance, the licensee opened a large junction box on instrument rack E-IR-67 to allow for calibrations and channel functional tests of pressure switches CIA-PS-21A, CIA-PS-22A and CIA-PS-39A. The inspectors observed portions of Procedure ISP-CIA-Q901 and identified that the junction box breached on instrument rack E-IR-67 served as a high energy line break barrier and was left unattended during the surveillance. The inspectors questioned if the environmental qualification and therefore the operability of the components located within instrument rack E-IR-67 were affected by the breached barrier. The inspectors also noted that instrument rack E-IR-67 contained additional components beyond those within the scope of Procedure ISP-CIA-Q901. The shift manager initiated Action Request AR 263187 to document the concerns involving the unattended barrier and requested engineering determine the impact of Procedure ISP-CIA-Q901 on all components located in instrument rack E-IR-67. Engineering evaluated Action Request AR 263187 and confirmed that the junction box opened on instrument rack E-IR-67 was a required high energy line break barrier. Environmentally qualified components within instrument rack E-IR-67 that were impacted by the unattended barrier included the pressure switches tested in Procedure ISP-CIA-Q901 and several safety-related pressure transmitters associated with the containment monitoring system.

For each of the components impacted, the licensee did not consider the effect of the unattended barrier on equipment operability or availability. During the May 6, 2012, performance of Procedure ISP-CIA-Q901, the licensee failed to meet requirements specified in Procedure PPM 1.3.57, Barrier Impairment," Revision 28. Step 4.1.7 of this procedure required the licensee to initiate a barrier impairment permit for high energy line break barriers that was breached on instrument rack E-IR-67 since the barrier was not continually manned such that it could be rapidly returned to an operable status upon observing a steam leak. Additionally, Step 4.13 of Procedure PPM 1.3.57 provided direction that high energy line break barriers are required to be operable in Modes 1, 2 and 3 and directed operations staff to initiate a barrier impairment permit and consider technical specification equipment inoperable for high energy line break barrier breaches.

For the May 6, 2012 surveillance, the licensee failed to declare inoperable and unavailable, all equipment impacted by the breached high energy line break barrier on instrument rack E-IR-67.

Following identification of this issue, the licensee determined the cause of the uncontrolled barrier to be a lack of alignment between the procedural requirements in Procedure PPM 1.3.57 and the individual work documents used to implement surveillance testing on equipment protected by hazard barriers. As an interim corrective action, the licensee initiated Night Order 1379 directing a more complete review of Procedure PPM 1.3.57 prior to work authorization on components that serve as hazard barriers. At the close of the inspection period, the licensee was evaluating more robust and long term corrective actions.

Analysis.

The failure to maintain control of required high energy line break barriers in accordance with Procedure PPM 1.3.57 was a performance deficiency. This performance deficiency was more than minor because it affected the configuration control attribute of the Mitigating Systems Cornerstone objective of ensuring the availability of systems that respond to initiating events. The inspectors performed an initial screening of the finding in accordance with IMC 0609.04, "Phase 1 - Initial Screening and Characterization of Findings." The inspectors determined this finding to be of very low safety significance (Green) because it did not result in the loss of a system safety function, did not represent the loss of safety function of a single train for greater than its allowed outage time, did not result in the loss of safety function of any non-technical specification equipment, and did not screen as potentially risk significant due to seismic, flooding, or severe weather initiating events. The inspectors determined that this finding had a cross-cutting aspect in the area of human performance associated with the resources component because the licensee failed to update surveillance procedures associated with high energy line break barriers such that individuals responsible for maintaining those barriers were knowledgeable of the requirements in Procedure PPM 1.3.57 H.2(c).

Enforcement.

Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures and Drawings," requires, in part, that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings. Licensee Procedure PPM 1.3.57, Barrier Impairment,"

Revision 28, Step 4.1.7, requires, in part, initiation of a barrier impairment permit for unattended breached high energy line break barriers or if the barrier cannot be rapidly returned to an operable status upon observing a steam leak or in the event an evacuation is required. Contrary to the above, on May 9, 2012, the licensee impaired the high energy line break barrier associated with instrument rack E-IR-67 without a barrier impairment permit and without meeting the requirement of Procedure PPM 1.3.57, Barrier Impairment," Revision 28, Step 4.1.7. Specifically, during performance of Surveillance Procedure ISP-CIA-Q901, ADS Accumulator Backup Low Pressure Alarm Division 1 CFT/CC," Revision 7, the high energy line break barrier associated with instrument rack E-IR-67 was left unattended and could not be rapidly restored to an operable status in the event of a steam leak. Because this violation was of very low safety significance (Green) and it was entered into the licensees corrective action program as Action Request AR 263187, this violation is being treated as a non-cited violation, consistent with the Enforcement Policy: NCV 05000397/2012003-03, Failure to Properly Control High Energy Line Break Barriers.

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation

Training Observations

a. Inspection Scope

The inspectors observed a simulator training evolution for licensed operators on May 8, 2012, which required emergency plan implementation by a licensee operations crew.

This evolution was planned to be evaluated and included in performance indicator data regarding drill and exercise performance. The inspectors observed event classification and notification activities performed by the crew. The inspectors also attended the postevolution critique for the scenario. The focus of the inspectors activities was to note any weaknesses and deficiencies in the crews performance and ensure that the licensee evaluators noted the same issues and entered them into the corrective action program. As part of the inspection, the inspectors reviewed the scenario package and other documents listed in the attachment.

These activities constitute completion of one sample as defined in Inspection Procedure 71114.06-05.

b. Findings

No findings were identified.

RADIATION SAFETY

Cornerstones: Public Radiation Safety and Occupational Radiation Safety

2RS0 1 Radiological Hazard Assessment and Exposure Controls

a. Inspection Scope

This area was inspected to:

(1) review and assess licensees performance in assessing the radiological hazards in the workplace associated with licensed activities and the implementation of appropriate radiation monitoring and exposure control measures for both individual and collective exposures,
(2) verify the licensee is properly identifying and reporting Occupational Radiation Safety Cornerstone performance indicators, and
(3) identify those performance deficiencies that were reportable as a performance indicator and which may have represented a substantial potential for overexposure of the worker.

The inspectors used the requirements in 10 CFR Part 20, the technical specifications, and the licensees procedures required by technical specifications as criteria for determining compliance. During the inspection, the inspectors interviewed the radiation protection manager, radiation protection supervisors, and radiation workers. The inspectors performed walkdowns of various portions of the plant, performed independent radiation dose rate measurements and reviewed the following items:

  • The hazard assessment program, including a review of the licensees evaluations of changes in plant operations and radiological surveys to detect dose rates, airborne radioactivity, and surface contamination levels
  • Instructions and notices to workers, including labeling or marking containers of radioactive material, radiation work permits, actions for electronic dosimeter alarms, and changes to radiological conditions
  • Programs and processes for control of sealed sources and release of potentially contaminated material from the radiologically controlled area, including survey performance, instrument sensitivity, release criteria, procedural guidance, and sealed source accountability
  • Radiological hazards control and work coverage, including the adequacy of surveys, radiation protection job coverage, and contamination controls; the use of electronic dosimeters in high noise areas; dosimetry placement; airborne radioactivity monitoring; controls for highly activated or contaminated materials (non-fuel) stored within spent fuel and other storage pools; and posting and physical controls for high radiation areas and very high radiation areas
  • Radiation worker and radiation protection technician performance with respect to radiation protection work requirements
  • Audits, self-assessments, and corrective action documents related to radiological hazard assessment and exposure controls since the last inspection Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one required sample as defined in Inspection Procedure 71124.01-05.

b. Findings

No findings were identified.

2RS0 3 In-plant Airborne Radioactivity Control and Mitigation

a. Inspection Scope

This area was inspected to verify in-plant airborne concentrations are being controlled consistent with ALARA principles, and the use of respiratory protection devices onsite do not pose an undue risk to the wearer. The inspectors used the requirements in 10 CFR Part 20, the technical specifications, and the licensees procedures required by technical specifications as criteria for determining compliance. During the inspection, the inspectors interviewed licensee personnel, performed walkdowns of various portions of the plant, and reviewed the following items:

  • The licensees use, when applicable, of ventilation systems as part of its engineering controls
  • The licensees respiratory protection program for use, storage, maintenance, and quality assurance of NIOSH certified equipment, qualification and training of personnel, and user performance
  • The licensees capability for refilling and transporting SCBA air bottles to and from the control room and operations support center during emergency conditions, status of SCBA staged and ready for use in the plant and associated surveillance records, and personnel qualification and training
  • Audits, self-assessments, and corrective action documents related to in-plant airborne radioactivity control and mitigation since the last inspection Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one sample as defined in Inspection Procedure 71124.03-05.

b. Findings

No findings were identified.

OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical Protection

4OA1 Performance Indicator Verification

.1 Data Submission Issue

a. Inspection Scope

The inspectors performed a review of the performance indicator data submitted by the licensee for the first quarter 2012 performance indicators for any obvious inconsistencies prior to its public release in accordance with Inspection Manual Chapter 0608, Performance Indicator Program.

This review was performed as part of the inspectors normal plant status activities and, as such, did not constitute a separate inspection sample.

b. Findings

No findings were identified.

.2 Safety System Functional Failures (MS05)

a. Inspection Scope

The inspectors sampled licensee submittals for the safety system functional failures performance indicator for the period from the first quarter 2011 through the first quarter 2012. To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, and NUREG-1022, Event Reporting Guidelines 10 CFR 50.72 and 50.73." The inspectors reviewed the licensees operator narrative logs, operability assessments, maintenance rule records, maintenance work orders, issue reports, event reports, and NRC integrated inspection reports for the period of January 2011 through March 2012 to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified.

Specific documents reviewed are described in the attachment to this report.

These activities constitute completion of one safety system functional failures sample as defined in Inspection Procedure 71151-05.

b. Findings

No findings were identified.

.3 Reactor Coolant System Specific Activity (BI01)

a. Inspection Scope

The inspectors sampled licensee submittals for the reactor coolant system specific activity performance indicator for the period from the first quarter 2011 through the first quarter 2012. To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6.

The inspectors reviewed the licensees reactor coolant system chemistry samples, technical specification requirements, issue reports, event reports, and NRC integrated inspection reports for the period of January 2011 through March 2012 to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified. In addition to record reviews, the inspectors observed a chemistry technician obtain and analyze a reactor coolant system sample. Specific documents reviewed are described in the attachment to this report.

These activities constitute completion of one reactor coolant system specific activity sample as defined in Inspection Procedure 71151-05.

b. Findings

No findings were identified.

.4 Reactor Coolant System Leakage (BI02)

a. Inspection Scope

The inspectors sampled licensee submittals for the reactor coolant system leakage performance indicator for the period from the first quarter 2011 through the first quarter 2012. To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6. The inspectors reviewed the licensees operator logs, reactor coolant system leakage tracking data, issue reports, event reports, and NRC integrated inspection reports for the period of January 2011 through March 2012 to validate the accuracy of the submittals.

The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the attachment to this report.

These activities constitute completion of one reactor coolant system leakage sample as defined in Inspection Procedure 71151-05.

b. Findings

No findings were identified.

.5 Occupational Exposure Control Effectiveness (OR01)

a. Inspection Scope

The inspectors reviewed performance indicator data for the second quarter 2011 through the first quarter 2012. The objective of the inspection was to determine the accuracy and completeness of the performance indicator data reported during these periods. The inspectors used the definitions and clarifying notes contained in NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, as criteria for determining whether the licensee was in compliance.

The inspectors reviewed corrective action program records associated with high radiation area (greater than 1 rem/hr) and very high radiation area non-conformances.

The inspectors reviewed radiological, controlled area exit transactions greater than 100 mrem. The inspectors also conducted walkdowns of high radiation areas (greater than 1 rem/hr) and very high radiation area entrances to determine the adequacy of the controls of these areas.

These activities constitute completion of one occupational exposure control effectiveness sample as defined in Inspection Procedure 71151-05.

b. Findings

No findings were identified.

.6 Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual

Radiological Effluent Occurrences (PR01)

a. Inspection Scope

The inspectors reviewed performance indicator data for the second quarter 2011 through the first quarter 2012. The objective of the inspection was to determine the accuracy and completeness of the performance indicator data reported during these periods. The inspectors used the definitions and clarifying notes contained in NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, as criteria for determining whether the licensee was in compliance.

The inspectors reviewed the licensees corrective action program records and selected individual annual or special reports to identify potential occurrences such as unmonitored, uncontrolled, or improperly calculated effluent releases that may have impacted offsite dose.

These activities constitute completion of one radiological effluent technical specifications/offsite dose calculation manual radiological effluent occurrences sample as defined in Inspection Procedure 71151-05.

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution

.1 Routine Review of Identification and Resolution of Problems

a. Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensees corrective action program at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed. The inspectors reviewed attributes that included the complete and accurate identification of the problem; the timely correction, commensurate with the safety significance; the evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root causes, extent of condition reviews, and previous occurrences reviews; and the classification, prioritization, focus, and timeliness of corrective actions. Minor issues entered into the licensees corrective action program because of the inspectors observations are included in the attached list of documents reviewed.

These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples. Instead, by procedure, they were considered an integral part of the inspections performed during the quarter and documented in Section 1 of this report.

b. Findings

No findings were identified.

.2 Daily Corrective Action Program Reviews

a. Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensees corrective action program. The inspectors accomplished this through review of the stations daily corrective action documents.

The inspectors performed these daily reviews as part of their daily plant status monitoring activities and, as such, did not constitute any separate inspection samples.

b. Findings

No findings were identified.

.3 Semi-Annual Trend Review

a. Inspection Scope

The inspectors performed a review of the licensees corrective action program and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors focused their review on repetitive equipment issues, but also considered the results of daily corrective action item screening discussed in Section 4OA2.2, above, licensee trending efforts, and licensee human performance results. The inspectors nominally considered the 6-month period of January 2012 through June 2012, although some examples expanded beyond those dates where the scope of the trend warranted.

The inspectors also included issues documented outside the normal corrective action program in major equipment problem lists, repetitive and/or rework maintenance lists, departmental problem/challenges lists, system health reports, quality assurance audit/surveillance reports, self-assessment reports, and Maintenance Rule assessments.

The inspectors compared and contrasted their results with the results contained in the licensees corrective action program trending reports. Corrective actions associated with a sample of the issues identified in the licensees trending reports were reviewed for adequacy.

These activities constitute completion of one single semi-annual trend inspection sample as defined in Inspection Procedure 71152-05.

b. Findings

The inspectors noted a trend in the reliability of emergency core cooling system keep fill pumps. Specifically, the following Action Requests were initiated within the assessment period documenting unexpected or emergent issues with emergency core cooling system keep fill pumps:

  • Action Request AR 256075, RHR-P-3 Vibration data shows pump bearing degradation
  • Action Request AR 257404, HPCS-P-3 Vibration Data shows pump bearings are degrading
  • Action Request AR 257708, HPCS-P-3 vibration degradation has increased
  • Action Request AR 258632, LPCS-P-2 making a cycling noise
  • Action Request AR 260533, High Vibration on RHR-P-3
  • Action Request AR 261113, Last RHR-P-3 Power Frame only lasted three months
  • Action Request AR 261816, LPCS-P-2 noise has increased Cause evaluation performed by the licensee under Action Request AR 261113 determined that tolerances within all of the emergency core cooling system keep fill pump frames have increased due to re-use and in-service time. Additionally, the improper sizing of the pump was identified as a contributor to premature bearing failure.

Corrective actions identified under Action Request AR 261113 include procurement of new, properly sized power frame units.

.4 Selected Issue Follow-up Inspection

a. Inspection Scope

During a review of items entered in the licensees corrective action program, the inspectors recognized a corrective action item (Action Request AR 260848) documenting procedure errors in Emergency Operating Procedure PPM 5.2.1, Primary Containment Control," Revision 19, and Severe Accident Guidelines Procedure SAG 2, Containment and Radioactivity Release Control," Revision 6. The procedure errors resulted in incorrect thresholds for venting primary containment when addressing possible hydrogen production within the plants primary containment.

These activities constitute completion of one in-depth problem identification and resolution sample as defined in Inspection Procedure 71152-05.

b. Findings

No findings were identified.

.5 In-depth Review of Operator Workarounds

a. Inspection Scope

On April 30, 2012, the inspectors reviewed the operations department burden list, control room deficiencies, and operator work around list to determine if any operator work arounds, either individually or collectively, could unnecessarily challenge mitigating system performance or operators during event response. The inspectors verified that Energy Northwest was identifying and documenting operator work around problems at an appropriate threshold. Documents reviewed are listed in the attachment.

These activities constitute completion of one sample as defined in Inspection Procedure 71152-05.

b. Findings

No findings were identified.

4OA3 Followup of Events and Notices of Enforcement Discretion

.1 (Closed) Licensee Event Report 2011-004-00, Secondary Containment Low Differential

Pressure Due to Ice Buildup On December 10, 2011, the control room received a secondary containment high differential pressure alarm. The alarm was due to a sudden in-rush of air into the reactor building. Action by the licensee to cut the reactor building outside air roll filters to address ice buildup caused the sudden in-rush of air. During this event, pressure in secondary containment briefly exceeded 0.0 inch water gauge. The secondary containment structure is normally maintained at negative 0.6 inch of water gauge during plant operations to ensure that any fission products are drawn into the structure, contained, and diluted before being released through the elevated plant stack. Limiting Condition for Operation 3.6.4.1, Secondary Containment, requires that secondary containment be operable during Modes 1, 2, and 3. Technical Specification Surveillance Requirement 3.6.4.1.1 requires the licensee verify secondary containment is less than negative 0.25 inch of water gauge every 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Based on the failure to meet the surveillance requirement, plant operators declared secondary containment inoperable and entered the applicable actions of Limiting Condition for Operation 3.6.4.1. Since secondary containment is a system required to control the release of radioactive material and mitigate the consequences of an accident and because the licensee failed to meet technical specification surveillance requirement due to secondary containment pressure being greater than negative 0.25 inch water gauge, secondary containment was inoperable and the event is reportable under 10 CFR 50.72(b)(3)(v)(C) and (D). The inspectors reviewed the licensee event report associated with this event and determined that the report adequately documented the summary of the event including the potential safety consequences and corrective actions required to address potential occurrences of icing in the future. No performance deficiencies were identified. This licensee event report is closed.

.2 (Closed) Licensee Event Report 2012-002-00, Technical Specification Non-Compliance

Due to Inadequate Procedure Guidance This licensee event report documents a technical specification action statement which was not entered and its associated required action was not completed. Specifically, the division 1 control room emergency filtration system was declared inoperable and Technical Specification Action Statement 3.7.3.B was entered. One of its required actions is to verify control room occupants will not be exposed to radiological hazards that will exceed the regulatory limits. Due to an inadequate procedure, the verification was not sufficient and Technical Specification Action Statement 3.7.3.C should have been entered. Technical Specification Action Statement 3.7.3.C Required Actions would have initiated a plant shutdown within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />, which did not occur. See Section 1R19 of NRC Inspection Report 05000397/2012002 for a discussion of an NRC identified finding associated with this issue. The inspectors completed a review of the licensee event report and did not identify any other violations of regulatory requirements or findings associated with this event. This licensee event report is closed.

4OA5 Other Activities

.1 (Closed) NRC Temporary Instruction (TI) 2515/177, Managing Gas Accumulation in

Emergency Core Cooling, Decay Heat Removal, and Containment Spray Systems (NRC Generic Letter 2008-01)

a. Inspection Scope

The inspectors evaluated whether the licensee maintained documents, installed system hardware, and implemented actions that were consistent with the information provided in their response to NRC Generic Letter 2008-01, Managing Gas Accumulation in Emergency Core Cooling, Decay Heat Removal, and Containment Spray Systems.

Specifically, the inspectors verified that the licensee had implemented, or was in the process of implementing, the commitments, modifications, and programmatically controlled actions described in their response to Generic Letter 2008-01. The inspectors conducted their review in accordance with Temporary Instruction 2515/177 and considered the site-specific supplemental information provided by the Office of Nuclear Reactor Regulation to the inspectors.

b. Inspection Documentation The inspectors reviewed the licensing basis, design, testing, and corrective actions as specified in the temporary instruction. The specific items reviewed and any resulting observations are documented below.

Licensing Basis: The inspectors reviewed selected portions of licensing basis documents to verify that they were consistent with the NRR assessment report, and that the licensee properly processed any required changes. The inspectors reviewed selected portions of technical specifications, technical specification bases, and the updated final safety analysis report. The inspectors also verified that applicable documents that described the plant and plant operation, such as calculations, piping and instrumentation diagrams, procedures, and corrective action program documents addressed the areas of concern and were changed, if needed, following plant changes.

The inspectors confirmed that the licensee performed surveillance tests at the frequency required by the technical specifications. The inspectors verified that the licensee tracked their commitment to evaluate and implement any changes that would be contained in the technical specification task force traveler.

Design: The inspectors reviewed selected design documents, performed system walkdowns, and interviewed plant personnel to verify that the licensee addressed design and operating characteristics. Specifically:

  • The inspectors verified that the licensee had identified the applicable gas intrusion mechanisms for their plant.
  • The inspectors verified that the licensee had established void acceptance criteria consistent with the void acceptance criteria identified by the Office of Nuclear Reactor Regulation. The inspectors also confirmed that the range of flow conditions evaluated by the licensee was consistent with the full range of design basis and expected flow rates for various break sizes and locations.
  • The inspectors selectively reviewed applicable documents, including calculations, and engineering evaluations with respect to gas accumulation in the high pressure core spray, low pressure core spray, residual heat removal, and drywell/wetwell spray systems. Specifically, the inspectors verified that these documents addressed venting requirements, aspects where pipes were normally voided, void control during maintenance activities, and the potential for vortex effects that could ingest gas into the systems during design basis events.
  • The inspectors conducted a walkdown of selected regions of the drywell/wetwell spray systems in sufficient detail to assess the licensees walk downs. The inspectors also verified that the information obtained during the licensees walkdown was consistent with the items identified during the inspectors independent walkdown.
  • The inspectors verified that piping and instrumentation diagrams and isometric drawings describe up-to-date configurations of the emergency core cooling systems and decay heat removal systems. The review of the selected portions of isometric drawings considered the following:

1. High point vents were identified.

2. High points without vents were recognizable.

3. Other areas where gas could accumulate and potentially impact operability, such as at orifices in horizontal pipes, isolated branch lines, heat exchangers, improperly sloped piping, and under closed valves, were described in the drawings or in referenced documentation.

4. Horizontal pipe centerline elevation deviations and pipe slopes in nominally horizontal lines that exceeded specified criteria were identified.

5. All pipes and fittings were clearly shown.

6. The drawings were up-to-date with respect to recent hardware changes, and that any discrepancies between as-built configurations and the drawings were documented and entered into the corrective action program for resolution.

  • The inspectors verified that the licensee had completed their walkdowns and selectively verified that the licensee-identified discrepant conditions in their corrective action program and appropriately modified affected procedures and training documents. The licensee identified to the inspector one portion of high pressure core spray that had not been walked down. The inspectors reviewed the evaluation for the portion of piping and determined that the region was bounded by the licensees analysis. The licensee informed the inspectors that the walk down would be performed at the next refueling outage.

Testing: The inspectors reviewed selected surveillances, post-modification tests, and post-maintenance test procedures and results, conducted during power and shutdown operations, to verify that the licensee was using procedures that appropriately addressed gas accumulation and/or intrusion into the subject systems. This review included the verification of procedures used for conducting surveillances and for the determination of void volumes to ensure that void criteria were satisfied and would continue to be satisfied until the next scheduled void surveillances. Also, the inspectors reviewed procedures used for filling and venting the following conditions that could introduce voids into the subject systems to verify that the procedures adequately tested for such voids and provided adequate instructions for their reduction or elimination.

Corrective Actions: The inspectors reviewed selected corrective action program documents to assess how effectively the licensee addressed the issues associated with Generic Letter 2008-01 in their corrective action program. In addition, the inspectors verified that the licensee implemented appropriate corrective actions for issues identified in the nine-month and supplemental responses. The inspectors determined that the licensee had effectively implemented the actions required by Generic Letter 2008-01.

Based on this review, the inspectors concluded that there is reasonable assurance that the licensee will complete all outstanding items and incorporate this information into the design basis and operational practices. This temporary instruction is closed for Columbia Generating Station.

c. Findings

No findings were identified.

4OA6 Meetings, Including Exit

Exit Meeting Summary

On May 10, 2012, the inspectors presented the inspection results for Temporary Instruction 2515/177 to Mr. M. Reddemann, Chief Executive Officer, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspectors confirmed that none of the potential report input discussed was considered proprietary.

On May 25, 2012, the inspectors presented the results of the radiation safety inspections to Mr.

C. King, Assistant Plant General Manager, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.

On July 2, 2012, the inspectors presented the inspection results to Mr. W. Hettel, Vice President, Operations, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.

4OA7 Licensee-Identified Violations

The following violations of very low safety significance (Green) were identified by the licensee and are violations of NRC requirements which meet the criteria of the NRC Enforcement Policy for being dispositioned as non-cited violations.

.1 Title 10 CFR, Part 50, Appendix B, Criterion III, Design Control, requires, in part, that

measures be established to assure that the design basis for structures, systems, and components are correctly translated into specifications, procedures, and instructions.

Contrary to the above, prior to April 10, 2012, the licensee failed to translate the correct flow coefficient for residual heat removal heat exchanger bypass valves RHR-V-48A and RHR-V-48B into Calculation 5.17.19 resulting in a calculated non-conservative pressure drop for the system. This non-conservative pressure drop was then translated into non-conservative acceptance criteria for Procedures OSP-RHR/IST-Q702, RHR Loop A Operability, Revision 0-33 and OSP-RHR/IST-Q703, RHR Loop B Operability Test, Revision 0-33. This finding was entered into the corrective action program as Action Request AR 261930. This finding was determined to be of very low safety significance because it represented a design or qualification deficiency confirmed not to result in a loss of operability.

.2 Technical Specification 5.4.1.a, Procedures, requires, in part, that written procedures

be established, implemented, and maintained as recommended in Regulatory Guide 1.33, Revision 2, Appendix A, dated February 1978. Paragraph 6 of Regulatory Guide 1.33, Appendix A, requires specific procedures for combating emergencies or other significant events. Contrary to the above, prior to April 6, 2012, licensee Procedure PPM 5.2.1, Primary Containment Control, Revisions 0-19 were inadequate because Table 27 of the procedure provided direction to vent primary containment based on values that were not consistent with the Offsite Dose Calculation Manual offsite radioactivity release limits. This finding was entered into the corrective action program as Action Request AR 260848. This finding was determined to be of very low safety significance because the procedure, as written, created a degraded condition that had potentially important implication for the integrity of containment, but would not have an impact on large early release frequency.

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

V. Bhardwaj, Manager, System Engineering
J. Brower, Supervisor, Design Engineering
E. Butler, Technician, Radiation Protection
B. Cook, Manager, Technical Training
M. Davis, Manager, Radiological Services
Z. Dunham, Supervisor, Licensing
G. Egert, Advisor, Health Physics Staff
D. Gregoire, Manager, Regulatory Affairs
T. Hancock, Supervisor, NSSS
P. Harness, Project Manager
M. Hedges, Licensing, Principal Engineer
W. Hettel, Vice President, Operations
A. Javorik, Vice President, Engineering
M. Kinmark, Advisor, Health Physics Staff
C. King, Assistant Plant General Manager,
D. Mand, Manager, Design Engineering
M. Reddemann, Chief Executive Officer
C. Sonoda, Engineer, Licensing
R. Shepherd, Operations Supervisor, Radiation Protection
K. Webb, Technician, Radiation Protection
S. Wellsfry, Gas Accumulation Program Owner

Attachment

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

None.

Opened and Closed

05000397-2012003-01 NCV Failure to Evaluate Operability Associated with Residual Heat Removal Pump B (Section 1R15)
05000397-2012003-02 NCV Failure to Establish Adequate Postmaintenance Tests for Replacement of Division 3 Safety Related Batteries (Section 1R19)
05000397-2012003-03 NCV Failure to Properly Control High Energy Line Break Barriers (Section 1R22)

Closed

05000397-2011-004-00 LER Secondary Containment Low Differential Pressure Due to Ice Buildup
05000397-2012-002-00 LER Technical Specification Non-Compliance Due to Inadequate Procedure Guidance

Discussed

None.

LIST OF DOCUMENTS REVIEWED