IR 05000397/2020004

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Integrated Inspection Report 05000397/2020004
ML21034A419
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 02/03/2021
From: Jeffrey Josey
NRC/RGN-IV/DRP
To: Sawatzke B
Energy Northwest
References
IR 2020004
Download: ML21034A419 (28)


Text

February 3, 2021

SUBJECT:

COLUMBIA GENERATING STATION - INTEGRATED INSPECTION REPORT 05000397/2020004

Dear Mr. Sawatzke:

On December 31, 2020, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Columbia Generating Station. On January 21, 2021, the NRC inspectors discussed the results of this inspection with Mr. G. Hettel, Chief Nuclear Officer/Vice President Nuclear Generation, and other members of your staff. The results of this inspection are documented in the enclosed report.

One finding of very low safety significance (Green) is documented in this report. This finding involved a violation of NRC requirements. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the NRC Resident Inspector at Columbia Generating Station.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the NRC Resident Inspector at Columbia Generating Station.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Jeffrey E. Josey, Chief Reactor Projects Branch A Division of Reactor Projects

Docket No. 05000397 License No. NPF-21

Enclosure:

As stated

Inspection Report

Docket Number:

05000397

License Number:

NPF-21

Report Number:

05000397/2020004

Enterprise Identifier: I-2020-004-0011

Licensee:

Energy Northwest

Facility:

Columbia Generating Station

Location:

Richland, WA

Inspection Dates:

October 01, 2020 to December 31, 2020

Inspectors:

L. Merker, Senior Resident Inspector

A. Patz, Senior Resident Inspector

W. Sifre, Senior Reactor Inspector

J. Vera, Resident Inspector

R. Alexander, Senior Emergency Preparedness Inspector

J. Drake, Senior Reactor Inspector

N. Hernandez, Operations Engineer

Approved By:

Jeffrey E. Josey, Chief

Reactor Projects Branch A

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Columbia Generating Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to Identify Gasket Critical Characteristic Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000397/2020004-01 Open/Closed

[H.12] - Avoid Complacency 71111.12 The inspectors identified a Green, non-cited violation (NCV) of 10 CFR Part 50, Appendix B,

Criterion III, associated with the licensees failure to establish measures for the selection and review for suitability of application of materials, parts, equipment, and processes that are essential to the safety-related functions of the structures, systems, and components.

Specifically, the licensee did not establish critical design characteristics for the control room emergency chiller 1B oil separator plate gasket, thus allowing installation of a gasket that did not meet the required width for proper component operation. The improper oil separator plate gasket did not prevent internal oil leakage from the compressor oil sump into the evaporator while in standby.

Additional Tracking Items

Type Issue Number Title Report Section Status URI 05000397/2020004-02 Reactor Core Isolation Cooling Drainpipe Steam Leak 71111.15 Open

PLANT STATUS

Columbia Generating Station began the inspection period at 100 percent power. On November 11, 2020, reactor power was reduced to 64 percent to perform maintenance on circulating water valve 2C. On November 14, 2020, the reactor was returned to 100 percent power. On November 20, 2020, plant power was reduced to 78 percent due to high-level trips of feedwater heaters 2B and 3B. On November 22, 2020, the reactor was returned to 100 percent power. On December 12, 2020, reactor power was reduced to 62 percent to perform control rod sequence exchanges, control rod scram time testing, turbine valve testing, main steam bypass valve testing, and planned maintenance on the adjustable speed drive 1B1 channel. The unit was returned to rated thermal power on December 13, 2020, where it stayed for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

Starting on March 20, 2020, in response to the National Emergency declared by the President of the United States on the public health risks of the Coronavirus Disease 2019 (COVID-19),resident inspectors were directed to begin telework and to remotely access licensee information using available technology. During this time, the resident inspectors performed periodic site visits each week; conducted plant status activities as described in IMC 2515, Appendix D, Plant Status; observed risk-significant activities; and completed on-site portions of IPs. In addition, resident and regional baseline inspections were evaluated to determine if all or portions of the objectives and requirements stated in the IP could be performed remotely. If the inspections could be performed remotely, they were conducted per the applicable IP. In some cases, portions of an IP were completed remotely and on-site. The inspections documented below met the objectives and requirements for completion of the IP.

REACTOR SAFETY

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1)residual heat removal system B following annual maintenance on October 22, 2020 (2)emergency chilled water system B following chiller 1B maintenance on November 19, 2020 (3)emergency chilled water system A following chiller 1B maintenance on November 19, 2020 (4)residual heat removal system A following annual maintenance on December 11, 2020

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (6 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1) Fire Area R-4/2, residual heat removal system B pump room, on October 20, 2020
(2) Fire Area SW-1/1, standby service water pumphouse 1A, on November 3, 2020
(3) Fire Area SW-2/2, standby service water pumphouse 1B, on November 3, 2020
(4) Fire Area ASD, adjustable speed drive building, on November 10, 2020
(5) Fire Area R-1/1, reactor building 548 foot elevation southeast quadrant, on November 12, 2020
(6) Fire Area R-5/1, residual heat removal system A pump room, on December 10, 2020

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated internal flooding mitigation protections in the residual heat removal systems A and B pump rooms on November 13, 2020.

71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance

Requalification Examination Results (IP Section 03.03) (1 Sample)

(1) The inspectors reviewed and evaluated the licensed operator examination failure rates for the annual requalification operating exam that was administered from November 2, 2020 to December 16, 2020.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the control room during a reactor downpower on November 11, 2020, to perform maintenance on circulating water valve 2C, and subsequent return to 100 percent power on November 14, 2020.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated licensed operator training for a station blackout event on October 14, 2020.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (2 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following SSCs remain capable of performing their intended function:

(1)residual heat removal system B on October 23, 2020 (2)residual heat removal system A on December 10, 2020

Quality Control (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated the effectiveness of maintenance and quality control activities to ensure the commercial dedication of the control room emergency chiller 1B oil separator plate gasket remained capable of performing its intended function on December 16, 2020.

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1)yellow risk for residual heat removal system B maintenance, week of October 19, 2020 (2)yellow risk for standby gas treatment system A maintenance, week of November 9, 2020 (3)yellow risk for residual heat removal system A maintenance, week of December 7, 2020

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (6 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1)control rod drive valve 10 stroke time exceeded action limit on October 4, 2020 (2)diesel generator 4 output breaker tripped outside of time tolerances during overcurrent trip testing on November 19, 2020 (3)loss of phase B voltage on 6.9kV switchgear bus E-SH-6 on November 30, 2020 (4)standby service water valve 226B failed leakage test on December 2, 2020 (5)residual heat removal valve 3A overthrust condition during diagnostic testing on December 18, 2020 (6)steam leak on reactor core isolation cooling system turbine inlet valve drain line on December 21, 2020

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (2 Samples)

The inspectors evaluated the following temporary or permanent modifications:

(1)circulating water valve 2C actuator removal, motor removal, and gag installation on November 20, 2020 (2)safety-related battery replacements; B2-1 (250 VDC), B1-1 (125 VDC), and B1-2 (125 VDC); on December 23, 2020

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the following post-maintenance test activities to verify system operability and functionality:

(1)residual heat removal system B on October 29, 2020 (2)scram discharge volume vent and drain valves on November 3, 2020 (3)standby gas treatment system A on November 16, 2020 (4)residual heat removal system A on December 9, 2020

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Surveillance Tests (other) (IP Section 03.01)

(1) ESB-B21-Q101, battery B2-1 (250 VDC) quarterly surveillance, on November 4, 2020
(2) OSP-ELEC-M701, diesel generator 1 monthly surveillance, on November 12, 2020
(3) OSP-FLEX-Q704, diesel generator 4 quarterly surveillance, on November 30, 2020

RCS Leakage Detection Testing (IP Section 03.01) (1 Sample)

(1) OSP-INST-H101, shift and daily instrument checks (Modes 1, 2, 3), on December 22, 2020

71114.02 - Alert and Notification System Testing

Inspection Review (IP Section 02.01-02.04) (1 Sample)

(1) The inspectors evaluated the maintenance and testing of the alert and notification system between January 1, 2019, and October 31, 2020.

71114.03 - Emergency Response Organization Staffing and Augmentation System

Inspection Review (IP Section 02.01-02.02) (1 Sample)

(1) The inspectors evaluated the readiness of the Emergency Preparedness Organization between January 1, 2019, and October 31, 2020.

71114.04 - Emergency Action Level and Emergency Plan Changes

Inspection Review (IP Section 02.01-02.03) (1 Sample)

(1) The inspectors evaluated the 10 CFR 50.54(q) emergency plan change process and practices between January 1, 2019, and October 31, 2020. This involved review of licensee screening and evaluation documentation. The reviews of the change process documentation do not constitute NRC approval.

71114.05 - Maintenance of Emergency Preparedness

Inspection Review (IP Section 02.01 - 02.11) (1 Sample)

(1) The inspectors evaluated the maintenance of the emergency preparedness program between January 1, 2019, and October 31, 2020.

71114.06 - Drill Evaluation

Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated simulator-based licensed operator requalification training (Crew F) on August 3,

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

EP01: Drill/Exercise Performance (IP Section 02.12)===

(1) January 1, 2019, through September 30, 2020

EP02: ERO Drill Participation (IP Section 02.13) (1 Sample)

(1) January 1, 2019, through September 30, 2020

EP03: Alert & Notification System Reliability (IP Section 02.14) (1 Sample)

(1) January 1, 2019, through September 30, 2020

BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10) (1 Sample)

(1) October 1, 2019, through September 30, 2020

BI02: RCS Leak Rate Sample (IP Section 02.11) (1 Sample)

(1) October 1, 2019, through September 30, 2020

71152 - Problem Identification and Resolution

Semiannual Trend Review (IP Section 02.02) (1 Sample)

(1) The inspectors reviewed the licensees corrective action program for potential adverse trends that might be indicative of a significant safety conscious work environment (SCWE) issue. The inspectors reviewed all anonymous action request reports for the period of March 2020, to November 2020 to identify potential SCWE issues.

Annual Follow-up of Selected Issues (IP Section 02.03) (3 Samples)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1)evaluation of the August 22, 2020, control rod 18-59 misposition event on October 9, 2020 (2)evaluation of the July 10, 2020, inverter 3A failure to transfer to inverter 3B event on December 18, 2020 (3)evaluation of external diverse and flexible mitigation capability (FLEX) equipment operating experience on December 28, 2020

71153 - Follow-up of Events and Notices of Enforcement Discretion Personnel Performance (IP Section 03.03)

(1) The inspectors evaluated the high-level trips of feedwater heater 2B and 3B, resultant reactor downpower to 78 percent, and the licensees response; November 20-21,

INSPECTION RESULTS

Failure to Identify Gasket Critical Characteristic Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems

Green NCV 05000397/2020004-01 Open/Closed

[H.12] - Avoid Complacency 71111.12 The inspectors identified a Green, non-cited violation (NCV) of 10 CFR Part 50, Appendix B, Criterion III, associated with the licensees failure to establish measures for the selection and review for suitability of application of materials, parts, equipment, and processes that are essential to the safety-related functions of the SSCs. Specifically, the licensee did not establish critical design characteristics for the control room emergency chiller 1B oil separator plate gasket, thus allowing installation of a gasket that did not meet the required width for proper component operation. The improper oil separator plate gasket did not prevent internal oil leakage from the compressor oil sump into the evaporator while in standby.

Description:

On June 19, 2020, control room emergency chiller 1B was shut down during surveillance testing due to low oil pressure. During their investigation, the licensee discovered metal debris in the oil. The licensee declared the chiller inoperable and performed a maintenance overhaul of the chiller from June 27-July 9, 2020. On July 3, 2020, the licensee unknowingly installed an incorrectly sized oil separator plate gasket. The licensee performed a 48-hour operability run and restored the chiller to operable status on July 11, 2020.

On July 13, 2020, an operator discovered the oil level in the compressor oil sump was lowering and entered this issue into the corrective action program under Action Request (AR)408654. The licensee added oil to restore oil level. Over the next few weeks, the licensee experienced repeated low oil levels; however, the licensee maintained the chiller operable by adding oil, doing multiple extended chiller runs, and performing an engineering evaluation.

The licensee performed a second major chiller overall and compressor internal inspection from August 6-17, 2020. On August 12, 2020, the incorrectly sized oil separator plate gasket was reinstalled. Over the next few weeks, the licensee again experienced repeated low oil levels; however, the licensee maintained the chiller operable based on multiple extended chiller runs and support from the previous engineering evaluation.

The licensee performed a third major chiller overall from September 13-October 4, 2020. On September 23, 2020, the licensee identified that an incorrectly sized oil separator plate gasket had been installed. On September 29, 2020, the licensee cut and installed a new gasket with the required width for proper component operation. The licensee restored control room emergency chiller 1B to operable status on October 4, 2020.

Title 10 CFR Part 21, Reporting of Defects and Noncompliance, establishes the framework for an acceptance process under the definition for dedication, to provide reasonable assurance that a commercial grade item to be used as a basic component will perform its intended safety function, and in this respect, is deemed equivalent to an item designed and manufactured under a 10 CFR 50, Appendix B, Quality Assurance program. This assurance is achieved by identifying the critical characteristics of the item and verifying their acceptability. Title 10 CFR 21.3, Definitions, defines critical characteristics, in part, as those important design, material, and performance characteristics of a commercial grade item that, once verified, will provide reasonable assurance that the item will perform its intended safety function. Title 10 CFR 21.3 also requires that the dedication process be conducted in accordance with the applicable provisions of 10 CFR Part 50 Appendix B, Quality Assurance Criteria for Nuclear Power Plants and Fuel Reprocessing Plants. Title 10 CFR Part 50, Appendix B, Criterion III, Design Control, includes the provisions for quality assurance and quality control which are applicable to the acceptance and dedication process for commercial-

-grade design and fulfills the Appendix B to 10 CFR Part 50 requirement established by the definition of dedication in 10 CFR Part 21 for commercial-grade dedication programs.

Criterion III requires, in part, that measures be established to assure that applicable regulatory requirements are correctly translated into specifications, drawings, procedures, and instructions; and that measures be established for the selection and review for suitability of application of materials, parts, equipment, and processes that are essential to the safety-related functions of the SSCs.

The inspectors noted that the gasket was a commercially-dedicated basic component.

During their review, the inspectors could not locate any specified critical characteristics (such as proper dimensions) in the licensees paperwork associated with the gasket other than a limitation on use statement that noted to verify proper size/fit at installation. The inspectors determined the licensee verified the part number supplied from the vendor and assumed the gasket was the correct size.

Corrective Actions: The licensees corrective actions included declaring control room emergency chiller 1B inoperable, performing an engineering analysis and starting the chiller to demonstrate operability, and replacing the incorrectly sized gasket.

Corrective Action References: ARs 408708, 409203, 411103, and 411140

Performance Assessment:

Performance Deficiency: The failure to establish measures for the selection and review for suitability of application of materials, parts, equipment, and processes that are essential to the safety-related functions of the SSCs was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Design Control attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the licensee did not establish critical design characteristics for the control room emergency chiller 1B oil separator plate gasket, thus allowing installation of a gasket that did not meet the required width for proper component operation. The improper oil separator plate gasket did not prevent internal oil leakage from the compressor oil sump into the evaporator while in standby.

Significance: The inspectors assessed the significance of the finding using Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors determined the finding was of very low safety significance (Green) because the finding was a deficiency affecting the design or qualification of a mitigating system, structure or component where operability or probabilistic risk assessment (PRA) functionality was maintained.

Cross-Cutting Aspect: H.12 - Avoid Complacency: Individuals recognize and plan for the possibility of mistakes, latent issues, and inherent risk, even while expecting successful outcomes. Individuals implement appropriate error reduction tools. This finding had a cross-cutting aspect in the area of human performance, avoid complacency, in that the licensee did not recognize and plan for the possibility of mistakes, latent issues, and inherent risk, even while expecting successful outcomes. Individuals implement appropriate error reduction tools. Specifically, the licensee verified the part number supplied from the vendor and assumed the gasket was the correct size.

Enforcement:

Violation: Title 10 CFR 21.3 requires, in part, that the dedication process be conducted in accordance with the applicable provisions of 10 CFR Part 50 Appendix B. Title 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires, in part, design control measures for the selection and the review for suitability of application of materials, parts, equipment, and processes that are essential to the safety-related functions of the SSCs.

Contrary to the above, on July 3, 2020, and August 12, 2020, the licensee failed to ensure the dedication process was conducted in accordance with the applicable provisions of 10 CFR Part 50, Appendix B, and establish measures for the selection and review for suitability of application of materials, parts, equipment, and processes that are essential to the safety-

-related functions of the SSCs. Specifically, the licensee did not establish critical design characteristics for the control room emergency chiller 1B oil separator plate gasket, thus allowing installation of a gasket that did not meet the required width for proper component operation. The oil separator plate gasket did not prevent internal oil leakage from the compressor oil sump into the evaporator while in standby.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Unresolved Item (Open)

Reactor Core Isolation Cooling Drainpipe Steam Leak URI 05000397/2020004-02 71111.15

Description:

An unresolved item was identified associated with a steam leak. On September 18, 2020, the licensee discovered a steam leak on the reactor core isolation cooling (RCIC) system turbine steam inlet valve drain line during recovery from a planned RCIC maintenance window. This issue was entered into the corrective action program under Action Request (AR) 410929. The licensee performed an operability determination that stated the RCIC system was operable with the steam leak because the leak was would not impact the required steam flow to the RCIC turbine. The licensee restored the RCIC system to normal standby lineup which isolated the steam leak on September 18, 2020.

On December 10, 2020, engineering entered AR 414023414023into the corrective action program with a concern that the operability determination from AR 410929410929failed to evaluate the steam leak against American Society of Mechanical Engineers (ASME) code requirements as the drain line was an ASME Section III, Class 2, high-energy pipe. Operations requested additional operability information from engineering to further evaluate operability of the RCIC system. The inspectors identified weaknesses in the additional operability information and determined the licensee needed to perform an ASME code repair on the pipe and submit an ASME code relief request to the NRC. On December 17, 2020, the licensee declared the RCIC system inoperable. On December 19, 2020, the licensee declared the RCIC system unavailable in order to perform the ASME code repair. The licensee restored the RCIC system to operable status on December 20, 2020. The licensee started an event investigation and entered AR 414343414343into the corrective action program to evaluate past operability of the RCIC system. Further review is necessary to determine whether a violation exists.

Planned Closure Actions: The inspectors need to evaluate whether the system turbine steam inlet valve drain line steam leak operability determinations were in violation of 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings" and whether the RCIC system was inoperable for longer than the Technical Specification 3.5.3 allowed outage timeframe of 14 days. The licensee is currently conducting an event investigation and past operability review. The inspectors will need to perform an independent review on past operability and evaluate the licensee's event investigation in order to determine whether a violation exists.

Licensee Actions: The licensee performed an ASME code repair on the turbine steam inlet valve drain line and is conducting an event investigation and past operability review.

Corrective Action References: ARs 410929, 414023, and 414343 Observation: Anonymous Action Requests Trends Identified 71152 The inspectors reviewed all anonymous action requests for the period of March 2020 to November 2020 to identify any potential safety conscious work environment issues. Two minor trends were identified: 1) low-level action items being submitted anonymously for the security group and 2) a continued technical discussion over multiple anonymous action requests. The inspectors noted that these issues would normally be expected to be addressed directly through the action request process, and that the originator being identified is useful in addressing such issues (for example, when reviewers seek clarification or additional details). These two trends could be low-level indicators of unwillingness to freely raise concerns through the corrective action process where the originator is identified. The inspectors discussed these trends with the plant Employee Concerns Program Manager, who indicated that they would consider taking actions to issue a communication to remind employees that they should feel free to raise concerns using the corrective action process.

EXIT MEETINGS AND DEBRIEFS

The inspectors confirmed that proprietary information was controlled to protect from public disclosure.

  • On November 5, 2020, the inspectors presented the emergency preparedness program inspection results to Mr. R. Schuetz, Site Vice President, and other members of the licensee staff.
  • On January 21, 2021, the inspectors presented the integrated inspection results to Mr.

G. Hettel, Chief Nuclear Officer/Vice President Nuclear Generation, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.04

Corrective Action

Documents

Action Requests

(ARs)

413950, 413997

Drawings

M521-1

Flow Diagram: Residual Heat Removal System Loop "A"

119

M521-2

Flow Diagram Residual Heat Removal Loop "B"

117

M524-1

Flow Diagram Standby Service Water System Reactor,

Radwaste, D.G. Bldg's and Yard

140

M775

Flow Diagram Emergency Chilled Water Piping System

Control Room

29

Procedures

1.3.29

Locked Valve Checklist

087

SOP-HVAC/CR-

LU

Control, Cable, and Critical Switchgear Rooms HVAC Lineup

001

SOP-RHR-LU

RHR System Valve and Breaker Lineup

009

SOP-RHR-STBY

Placing RHR in Standby Status

005

SOP-SW-LU

Standby Service Water System Valve and Breaker Lineup

014

71111.05

Calibration

Records

FP-02-85-03

Combustible Loading Calculation

010

Fire Plans

PFP-RB-422

Reactor 422

006

Procedures

1.3.10

Plant Fire Protection Program Implementation

036

1.3.10C

Control of Combustibles

2

1.3.57

Barrier Impairment

039

ABN-FIRE

Fire

041

PFP-MN-XFMR-

YD-MISC

MN XFMR YD Misc Bldgs

007

71111.06

Calculations

ME-02-02-02

Reactor Building Flooding Analysis

004

Corrective Action

Documents

Action Requests

(ARs)

2045

71111.06

Drawings

M539

Flow Diagram Floor Drain System Reactor Building

090

M723

Embedded Floor & Equipment Drains - Reactor Building

Elevation 422 - 3

005

Miscellaneous

BIP 17-0406

Barrier Impairment Permit to Remove and Reinstall the Floor

Plugs to Support FDR-AO-221 Work

11/03/2020

Procedures

10.2.101

Informational Visual Examinations

005

10.2.208

Borg Warner Gate Valve Model 401HBC6-003 with Magna

Thrust Operator

2

10.2.251

Installation of Temporary Flood Barriers

000

ABN-FLOODING

Flooding

2

OSP-FDR/IST-

Q702

FDR Secondary Containment Valve Operability

006

Work Orders

2145870, 02109343, 02152587

71111.11Q Corrective Action

Documents

Action Requests

(ARs)

2246, 412947, 412961, 412964

Engineering

Changes

18557

CW-V-2C Gag Temp Mod

000

Miscellaneous

Control Rod Withdrawal Deviation Sheet

11/11/2020;

11/13/2020

Reactivity Control Plan to Recover from Circ Water Valve

Repair - November 2020

11/11/2020

Procedures

13.1.1

Classifying the Emergency

047

3.2.6

Power Maneuvering

015

4.603.A8

603.A8 Annunciator Panel Alarms

043

5.6.1

SBO/ELAP Chart

030

5.6.2

Station Blackout SBO and Extended Loss of AC Power ELAP

Attachments

015

9.3.12

Plant Power Maneuvering

037

9.3.9

Control Rod Withdrawal Sequence Development and Control

030

ABN-CORE

Unplanned Core Operating Conditions

018

ABN-ELEC-LOOP Loss of All Offsite Electrical Power

017

ABN-

TRANSFORMER

Transformer Abnormal Operation

26

SOP-CR-

MOVEMENT

Control Rod Movement

004

71111.12

Corrective Action

Documents

Action Requests

(ARs)

410313, 412073, 412115, 408708, 409203, 411103, 411140,

411639, 413950, 413964, 413949, 413955, 413945, 413873,

2326, 388782, 390620, 332326, 396010, 372892, 396502

Miscellaneous

CGS RHR System Health Report dated November 4, 2020

BIP 20-0195

Barrier Impairment for ISP-RHR-X304

10/20/2020

PL-0002

Standard Procurement and Use Policy for Gaskets

28

Procedures

1.10.11

Technical Assessments Supporting Reportability and

Reportability Evaluations

2

1.3.64

Plant Clearance Order

044

1.5.11

Maintenance Rule Program

016

10.2.10

Fastener Torque and Tensioning

28

10.25.105

Motor Control Center and Switchgear Maintenance

039

10.25.13A

4.16KV Vacuum Breaker Maintenance and Stored Energy

Mechanism

21

10.25.168

Maintenance and Repair of Limitorque Valve Operators -

Model SMB and SB 0 Through 4

013

3.4.1

Minimizing the Potential of Draining the Reactor Vessel -

Water Inventory Control

21

ISP-RHR-X304

ECCS-LPCI (B and C) Pump Discharge Low (Minimum Flow) -

CC

008

MWES-2

Engineering Standards for Standard Recommended Practice

004

SPES-1.6.17

Procurement Specifications

055

SPES-1.6.5

Commercial Grade Dedication

050

SPES-1.7.41

Critical Characteristic/Equipment Concerns

046

SPES-1.9

9.0 Appendixes [sic]

055

SQI-10-3

Receiving Inspection

2

SQI-18-4

Commercial Grade Item Survey

009

SQI-7-2

Evaluation of Suppliers

2

SWP-PUR-02

Procurement Technical Reviews

010

SWP-PUR-04

Material, Equipment, Parts, and Supplies Procurement

016

SYS-4-31

System and Equipment Performance Monitoring and Trending

Program

2

WCI-2

Standard Operating Cycle Schedule Development

006

Work Orders

2168795, 02115864, 02135659, 02139791, 02161200,

2153094, 02152781, 02160160, 02160196, 02168795,

2039377, 02124750, 02107556, 02169507, 02149765,

2159074, 02146580, 02110027, 02111170, 02149765

71111.13

Corrective Action

Documents

Action Requests

(ARs)

2851, 412858, 412859, 412901

Corrective Action

Documents

Resulting from

Inspection

2066

E-TR-IN/2 buzzing

10/19/2020

2116

Transient combustible permit expired

10/20/2020

2117

Transient combustible permit inaccurate

10/20/2020

Miscellaneous

Operator Logs: December 7 - 8, 2020

2/08/2020

BIP 20-0325

Barrier Impairment Permit for PPM 15.1.17 Ventilation Air

Flow Test

11/10/2020

BIP 20-0555

Barrier Impairment Permit for Propping Door R614 Open

2/08/2020

FSIP 20-0207

Fire System Impairment Permit for Standby Gas Treatment

System A Filter Unit 1A

11/10/2020

Procedures

1.3.10

Plant Fire Protection Program Implementation

036

1.3.10C

Control of Combustibles

2

1.3.57

Barrier Impairment

039

1.3.76

Integrated Risk Management

060

1.3.83

Protected Equipment Program

2

1.5.14

Risk Assessment and Management for

Maintenance/Surveillance Activities

043

Work Orders

2161050, 02104163, 02131361, 02111170

71111.15

Calculations

E/I-02-95-01

Overcurrent Protective Device Settings & Coordination

Calculation for 480 Volt Distribution Systems

007

ME-02-01-30

Determination of RCIC Availability without Standby Service

Water

000

ME-02-92-43

Room Temperature Calculation for DG Building, Reactor

Building, Radwaste Building and Service Water

013

RCIC-1482-1

Drain from RCIC-DT-1 to Drip Leg

2

RCIC-1482-2

Drain from RCIC-DT-1 to Drip Leg

2

71111.15

Corrective Action

Documents

Action Requests

(ARs)

2595, 372062, 372279, 397571, 411575, 409695, 409856,

409857, 410954, 411040, 391735, 393301, 393370, 403897,

413171, 413175, 413474, 412247, 413950, 410929, 414023

Drawings

317-00,2130

Drain from RCIC-DT-1 to Drip Leg

010

EWD-3E-017

Electrical Wiring Diagram Reactor Recirculation System 6.9kV

SWGR E-SH-6 BRDR RRC-CB-RRB

014

EWD-46E-042

Electrical Wiring Diagram AC Electrical Distribution Systems

6.9kV Bus 6 and E-TR-S X Winding UNDV

009

M519

Flow Diagram: Reactor Core Isolation Cooling

103

M775

Flow Diagram Emergency Chilled Water Piping System

Control Room

29

Engineering

Changes

17708

Diesel Generator 4 (DG4) Output Breaker Replacement

001

18566

TMOD Remove SH-6 UV Relay E-RLY-27/6

000

Miscellaneous

AED SPC 1

ASME Piping Systems

24

RHR-MO-3A

MOV Master Data Sheet

009

RHR-MO-3A

Overthrust Evaluation

2/08/2020

TM-2150

Mission Time of Emergency Safety Features

001

Procedures

1.3.66

Operability Determination

036

1.5.1

Surveillance Testing Program

043

MES-3

Piping Design Guide

005

OSP-CCH/IST-

M702

Control Room Emergency Chiller System B Operability

045

OSP-CRD/IST-

Q701

Scram Discharge Volume Vent and Drain Valves Operability

008

OSP-RHR/IST-

Q702

RHR Loop A Operability Test

053

Work Orders

2119234, 02163216, 02170796, 02170824, 02155871,

2145984, 29157385, 29157394, 02077609, 02151526,

2172876, 29157097, 02126182, 02171498, 02159074,

2169507, 02172942

71111.18

Corrective Action

Documents

Action Requests

(ARs)

407479, 412859, 412915, 412988, 393512, 393661, 402407,

403247, 407256, 407800, 408773, 409608, 412116, 412117

Engineering

Changes

204

TMOD for Online Station Battery E-B2-1 Replacement

000

18317

TMOD for Online Station Battery E-B1-1 and E-B1-2

Replacement

000

18557

CW-V-2C Gag Temp Mod

000

Miscellaneous40-000,47

Butterfly Valves & Operators Owner's Manual

2

ISP 20-0204

Ignition Source Permit for CW-V-2C Welding

11/13/2020

TCP 20-0198

Transient Combustible Permit for CW-V-2C

11/13/2020

Procedures

1.3.57

Barrier Impairment

039

1.3.9

Temporary Modifications

057

10.2.226

Mechanically Gagging Equipment

2

10.25.219

Online Battery Replacement of 125 VDC E-B1-1

000

10.25.230

Online Battery Replacement of 125 VDC E-B1-2

000

10.25.236

Online Battery Replacement of 250 VDC E-B2-1

000

SWP-DES-01

Plant Modifications & Configuration Control

017

Work Orders

2172415, 02091531, 02115649, 02124385, 02157379

71111.19

Corrective Action

Documents

Action Requests

(ARs)

2115, 412073, 412159, 373358, 411575, 412368, 412378,

2823, 412890, 412901, 412661

Miscellaneous

Operations Department Narrative Logs for December 9, 2020

BIP 20-0325

Barrier Impairment Permit for PPM 15.1.17 Ventilation Air

Flow Test

11/10/2020

BIP 20-0418

Barrier Impairment Permit to Open Doors of SGT-FU-1A

11/11/2020

FSIP 20-0207

Fire System Impairment Permit to Isolate & Test Deluge

Nozzles per PPM 15.1.17

11/10/2020

Procedures

15.1.17

Ventilation Deluge Systems Air Flow Test

017

OSP-CRD/IST-

Q701

Scram Discharge Volume Vent and Drain Valves Operability

008

OSP-RHR-M102

RHR B Fill Verification

2

OSP-RHR/IST-

Q702

RHR Loop A Operability Test

053

OSP-RHR/IST-

Q703

RHR Loop B Operability Test

060

OSP-SGT-M701

Standby Gas Treatment System A Operability

018

71111.19

Procedures

OSP-SGT/IST-

Q701

SGT Valve Operability (System A)

010

SWP-TST-01

Post Maintenance Testing Program

017

Work Orders

2115864, 02156981, 02134952, 02168795, 02163216,

2170824, 02170796, 02104163, 02112327, 02131362,

2161050, 02161072, 02169507, 02149765, 02159074

71111.22

Corrective Action

Documents

Action Requests

(ARs)

2774, 369958, 312509, 410018, 411138, 411854, 414249

Miscellaneous

Instrument Master Data Sheet for FDR-FQ-38

003

CVI 02-51A-00

Exide Instruction Manual

008

Procedures

8.4.54

Thermal Performance Monitoring of DCW-HX-1A1 and DCW-

HX-1A2

010

ESP-B21-Q101

Quarterly Battery Testing 250VDC E-B2-1

013

ISP-FDR/EDR-

M401

Drywell Sump Flow Monitors - CFT

007

ISP-FDR/EDR-

X301

Drywell Sump Flow Monitors - CC

011

OSP-DO-Q701

DO-P-1A Operability

001

OSP-ELEC-W101

Offsite Station Power Alignment Check

2

OSP-FDR/IST-

Q701

FDR Valve Operability

004

OSP-FLEX-Q704

Diesel Generator 4 Quarterly Surveillance

000

OSP-INST-H101

Shift and Daily Instrument Checks (Modes 1, 2, 3)

094

SOP-FDR-OPS

Floor Drain System Operation

003

TSP-DG1-X501

DG1 Shutdown Logic Checks

003

Work Orders

2134491, 02134497, 02136100, 02160766, 02168151,

29156291, 02163167, 02135995

71114.02

Corrective Action

Documents

Action Requests

(AR)

391263, 391789, 392263, 392551, 400727, 403397, 406956,

407353

Corrective Action

Documents

Resulting from

Inspection

Action Requests

(AR)

2662

Miscellaneous

Alert and Notification System (ANS) Design Report - Revision

11/14/2016

CGS ANS Annual Report for 2019 (to FEMA Region X)

01/29/2020

Procedures

TSI-6.2.22

EP Annual Emergency Response Siren System Activation

Test

004

TSI-6.2.32

EP Siren Polling Test

003

TSI-6.2.48

EP Siren Site Inspections

2

TSI-6.2.49

EP River Siren Post-Maintenance Test

001

TSI-6.3.8

EP ANS System Battery Replacements

000

Work Orders

WO 02125942-01

EP Inspect Siren Sites (per TSI-6.2.48)

05/20/2020

WO 02171707-01

ESSN Perform Siren System Polling Test (per TSI-6.2.32)

11/04/2020

71114.03

Corrective Action

Documents

Action Requests

(AR)

2339, 396868, 400339, 401462, 4040980, 407465, 408060

Corrective Action

Documents

Resulting from

Inspection

Action Requests

(AR)

2612, 412757

Miscellaneous

Quarterly Off-Hours ERO Notification Drill Results (per EPI-19) 1Q/2019,

2Q/2019,

3Q/2019,

1Q/2020,

2Q/2020,

3Q/2020

Annual Unannounced ERO Call Out Drill (per EPI-19,

conducted 11/6/2019)

11/14/2019

EP-02

CGS ERO On-Shift Staffing Analysis Report (Rev 3)

07/08/2018

Procedures

13.10.1

Control Room Operation and Shift Manager Duties

035

13.4.1

Emergency Notifications

044

EPC 26045

Energy Northwest Emergency Classification or Other

Emergency Messages

036

EPI-19

Communications Tests

010

OI-34

Notifications

039

SWP-EPP-01

Emergency Response Organization and Training

2

71114.04

Corrective Action

Documents

Action Requests

(AR)

389508, 390488

Miscellaneous

2019 50.54(q) Tracking Log

20 50.54(q) Tracking Log

Tracking No.

2019-03

50.54(q) Screen - All EPIPs in Attachment 4 of CGS

Emergency Plan (Update to References)

03/18/2019

Tracking No.

2019-13

50.54(q) Screen for PPM 13.14.9, Emergency Program

Maintenance, Revision 30

05/07/2019

Tracking No.

2019-18

50.54(q) Screen for PPM 13.10.8, Security Lieutenant and

Security Force Duties, Revision 26; and EPC 26573, SCC

Duty Officer Checklist, Revision 8

10/01/2019

Tracking No.

2019-18

§ 50.54(Q) Change Evaluation for PPM 13.10.8, Security

Lieutenant and Security Force Duties, Revision 26

10/02/2019

Tracking No.

20-15

50.54(q) Screening for PPM 13.8.1, Emergency Dose

Projection System Operations, Revision 39, Minor Revision 05

03/17/2020

Procedures

EPI-16

§ 50.54(Q) Change Evaluation

016

71114.05

Corrective Action

Documents

Action Requests

(AR)

388485, 388568, 390016, 390017, 392049, 394205, 395491,

397304, 397614, 397852, 398002, 398872, 399147, 399484,

401722, 402961, 403544, 403778, 403836, 404033, 404038,

404211, 404328, 405708, 405883, 407302, 407305, 407311,

407313, 407353, 407561, 407596, 409240, 412623,

Miscellaneous

Memorandum of Understanding Between Energy Northwest

and

U.S. Department of Energy, Richland Operations Office,

for Emergency Preparedness and Response

10/09/2020

Memorandum of Understanding Between Framatome Inc. and

Energy Northwest October 2018

11/09/2018

Letter of Agreement Between Energy Northwest and Kadlec

Regional Medical Center

10/30/2012

ERO Team B Drill Report - August 25, 2020

09/29/2020

ERO Team D Dress Rehearsal Drill Report - February 25,

20

03/19/2020

8-Year Exercise Cycle Element Tracking

10/20/2020

71114.05

Miscellaneous

Plant Health Committee Presentation - Emergency

Preparedness System Health Report Summary

09/15/2020

ERO Team A Drill Report - September 10, 2019

10/10/2019

ERO Team B Drill Report - July 16, 2019

08/06/2019

ERO Team C Drill Report - February 19, 2019

2/19/2019

ERO Team D Drill Report - October 29, 2019

11/26/2019

2019 Field Sampling Team Drill Report

10/15/2019

AR 388340388340EP Department MOU Review Tracker - 2019

AR 388343388343On-Site Medical Emergency Drill 2019 - Contaminated/Injured

Man

09/03/2019

AR 388355-03

2019 Fire Drill with Hanford Fire Department

2/12/2019

AR 3986873986872019 Chemistry Liquid Sampling Drill Report

2/03/2019

AR 40083640083620 Emergency Preparedness Program 12-Month Audit

Frequency Evaluation (50.54(t) Review)

2/06/2020

AR 40282940282920 Field Team Monitoring Sampling Team Drill

01/22/2020

AU-EP-19

Quality Services Audit Report: Emergency Preparedness

Program (50.54(t) Review)

03/14/2019

EP-01

Emergency Plan - Columbia Generating Station

066, 067

EP-03

Development of Evacuation Time Estimates, Rev. 0

10/2012

KLD TR-1106

Columbia Generating Station: 2019 Population Update

Analysis

09/25/2019

KLD TR-1186

Columbia Generating Station: 2020 Population Update

Analysis

09/23/2020

Procedures

13.1.1A

Classifying The Emergency - Technical Bases

034

13.10.2

TSC Manager Duties

035

13.10.9

Operations Support Center Manager and Staff Duties

050

13.11.1

EOF Manager Duties

044

13.14.11

EP Equipment

014

13.14.8

Drill and Exercise Program

018

13.14.9

Emergency Program Maintenance

030

13.2.2

Determining Protective Action Recommendations

20

EPI-17

After Action Report / Improvement Plan Formatting,

Distribution, and Retention

008

EPI-21

Drill and Exercise Development and Implementation

019

71114.05

Procedures

SWP-CAP-01

Corrective Action Program

2

SWP-CAP-06

Condition Report Review

27

Self-Assessments SA 371289

Focused Self-Assessment Report: Emergency Preparedness

Exercise Year Self-Assessment

2/03/2019

SA 386590

Snap-Shot Self-Assessment Report: Columbia Generating

Station Emergency Preparedness Non-Exercise Year

10/01/2020

Work Orders

WO 02142631-01

ICP-MET-S302: Meteorological Rain Gauge & Temperature

Monitoring Instrumentation Channel Calibration

10/01/2019

WO 02145979-01

AMA-AH-51 Will Not Maintain Temperatures in TSC

08/28/2019

WO 02160278-01

Replace and Test ARM-RE-34

08/12/2020

WO 02163515-01

Replace MET-TE 10A, 10B, 11A and 11B: ICP-MET-S302

07/08/2020

WO 02165339-01

Received 602.A5.1-1 Refuel Floor Area Rad High Alarm

10/16/2020

71114.06

Corrective Action

Documents

Action Requests

(ARs)

409496

Miscellaneous

AOM-T Roll-up Comments: Cycle 20-04

000

Crew F 4.0 Critique Summary LR002492

08/03/2020

Drill, Exercise, and Actual Events Opportunity Crew F

Evaluation: Event 2020-15

08/03/2020

Form 24075

Columbia Generating Station Classification Notification Form

(CNF)

24

Form 25665

Reactor Plant Event Notification Worksheet Form

004

Form 26045

Energy Northwest Emergency Classification or Other

Emergency Messages Form

036

Form 26051

Energy Northwest Public Address Emergency Message for

Site Evacuation Form

013

LR002492

Cycle 20-4 Evaluated Scenario

000

Procedures

13.1.1

Classifying the Emergency

049

13.1.1A

Classifying the Emergency - Technical Bases

034

13.2.2

Determining Protective Action Recommendations

20

13.4.1

Emergency Notifications

044

13.5.1

Local, Protected Area or Site Evacuation

031

EP-01

Emergency Plan Columbia Generating Station

067

EPI-18

Emergency Preparedness Performance Indicators

27

71151

Corrective Action

Documents

Action Requests

(AR)

391263, 391789, 396911, 402143

Action Requests

(ARs)

400472

Corrective Action

Documents

Resulting from

Inspection

Action Requests

(AR)

2568

Miscellaneous

Monthly Key ERO Member Qualification Records

1Q/2019 -

3Q/2020

Select DEP PI Opportunity Assessments: 2019-04, 2019-05,

2019-09, 2019-14, 2019-16, 2019-18, 2019-20, 2019-27,

2019-32, 2020-08, 2020-11, 2020-12, 2020-13, 2020-14,

20-15, 2020-16

Operations Logs

10/01/2019 -

09/30/2020

Procedures

CI-10.17

Iodine

2

CSP-I131-W101

Reactor Coolant Isotopic Analysis for I-131 Dose Equivalent

009

EPI-18

Emergency Preparedness Performance Indicators

27

OSP-INST-H101

Shift and Daily Instrument Checks Modes 1, 2, 3

094

Work Orders

2120129, 02135838

71152

Corrective Action

Documents

Action Requests

(ARs)

410059, 410060, 410066, 410067, 410096, 411554, 411765,

405158, 405159, 405652, 406513, 407846, 408060, 408789,

409527, 409528, 409529, 409530, 409585, 409586, 409587,

409729, 409730, 409731, 409732, 409733, 409734, 410509,

410834, 410850, 410967, 412918, 413001, 413080, 413262,

408616, 408620, 408622, 408656, 408724, 408741, 410656,

410659, 410677, 410717, 410720, 413485, 368369, 390048,

404936, 406864

Drawings

E504-1

Vital One Line Diagram

006

Engineering

Changes

17708

Diesel Generator 4 (DG4) Output Breaker Replacement

001

Miscellaneous

Technical Issue Resolution Cause Evaluation Sheet for E-

ATS-IN/3

09/29/2020

71152

Miscellaneous

Technical Issue Resolution Fact Sheet for E-ATS-IN/3

09/29/2020

Operator Logs: August 21 - 23, 2020

10/08/2020

Columbia Nuclear Generating Plant - Nuclear Safety Culture

Assessment March 9 - 13, 2020

04/20/2020

Procedures

1.3.84

Reactivity Management Control

006

10.25.1

Inspections and Cleaning Division 1, E-IN-3A and E-IN-3B,

and Division 2, E-IN-2A and E-IN-2B, Inverters

27

4.800.C1

800.C1 Annunciator Panel Alarms

031

ABN-ELEC-INV

20 VAC Critical Distribution System Failures

017

ABN-ROD

Control Rod Faults

031

FLEX-01

FLEX Program

003

OI-09

Operations Standards and Expectation

078, 079

OPEX-01

Operating Experience Program Implementation Manual

010, 011

OSP-CRD-M701

Control Rod Exercise

27, 028

SOP-CR-

MOVEMENT

Control Rod Movement

003, 004

SOP-ELEC-IN3-

OPS

IN3 Operations

013, 014

SWP-CAP-01

Correction Action Program

041, 042

SWP-OPX-01

Operating Experience Program

001

Work Orders

2157506, 29155689, 29155696, 29156799, 29156806,

2131744, 02151530, 02166850, 02148039

71153

Drawings

M503

Flow Diagram Extraction Steam & Heater Vents Turbine

Generator Building

016

M505-1

Flow Diagram Heater Drain System Turbine Generator

Building

21

M505-2

Flow Diagram Heater Drain System Turbine Generator

Building

015

Procedures

ABN-FWH-

HILEVEL/TRIP

Feedwater Heater High-Level Trip

007

SOP-MSR-OPS

Main Turbine Moisture Separator Reheater Operations

010

Work Orders

2172871