IR 05000333/2012005

From kanterella
Jump to navigation Jump to search
IR 05000333012-005; 10/01/2012 - 12/31/2012; James A. FitzPatrick Nuclear Power Plant (FitzPatrick); Follow-Up of Events
ML13038A174
Person / Time
Site: FitzPatrick Constellation icon.png
Issue date: 02/07/2013
From: Burritt A L
Reactor Projects Branch 2
To: Colomb M J
Entergy Nuclear Northeast
References
IR-12-005
Download: ML13038A174 (51)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION REGION I 2100 RENAISSANCE BOULEVARD, SUITE 100 KING OF PRUSSIA, PENNSYLVANIA 19406-2713 February 7, 2013 Mr. Michael Site Vice President Entergy Nuclear Northeast James A. FitzPatrick Nuclear Power Plant P. O. Box 110 Lycoming, NY 13093

SUBJECT: JAMES A. FITZPATRICK NUCLEAR POWER PLANT - NRC INTEGRATED INSPECTION REPORT 05000333/2012005

Dear Mr. Colomb:

On December 31, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your James A. FitzPatrick Nuclear Power Plant (FitzPatrick). The enclosed inspection report documents the inspection results which were discussed on January 18, 2013, with you and members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

The report documents two findings of very low safety significance (Green). These findings were also determined to involve violations of NRC requirements. However, because of the very low safety significance and because they are entered into your corrective action program, the NRC is treating these findings as non-cited violations (NCVs) consistent with Section 2.3.2 of the NRC Enforcement Policy. If you contest any NCVs in this report, you should provide a response within 30 days of the date of the inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington, DC 20555-

0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Senior Resident Inspector at FitzPatrick. In addition, if you disagree with the cross-cutting aspect assigned any finding in this report; you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region I, and the NRC Senior Resident Inspector at FitzPatrick.

In accordance with 10 CFR Part 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible from the NRC website at http://www.nrc.gov/reading-rm/adams.html the Public Electronic Reading Room).

Sincerely,/RA/ Arthur L. Burritt, Chief Reactor Projects Branch 2 Division of Reactor Projects Docket No.: 50-333 License No.: DPR-59

Enclosure:

Inspection Report 05000333/2012005

w/Attachment:

Supplementary Information cc w/encl: Distribution via ListServ

SUMMARY OF FINDINGS

........................................................................................................... 3

REPORT DETAILS

REACTOR SAFETY

............................................................................................................. 5 1R01 Adverse Weather Protection ................................................................................ 5

1R04 Equipment Alignment ........................................................................................... 6 1R05 Fire Protection ...................................................................................................... 7 1R11 Licensed Operator Requalification Program ........................................................ 8

1R12 Maintenance Effectiveness .................................................................................. 9

1R13 Maintenance Risk Assessments and Emergent Work Control ............................ 9

1R15 Operability Determinations and Functionality Assessments .............................. 10 1R18 Plant Modifications ............................................................................................. 11 1R19 Post-Maintenance Testing ................................................................................. 11

1R20 Refueling and Other Outage Activities ............................................................... 12

1R22 Surveillance Testing ........................................................................................... 13

RADIATION SAFETY

......................................................................................................... 14

2RS1 Radiological Hazard Assessment and Exposure Controls ................................. 14

2RS2 Occupational ALARA Planning and Controls ..................................................... 18

2RS3 In-Plant Airborne Radioactivity Control and Mitigation

OTHER ACTIVITIES

.......................................................................................................... 20

4OA1 Performance Indicator Verification ..................................................................... 20

4OA2 Problem Identification and Resolution ............................................................... 22

4OA3 Follow-Up of Events and Notices of Enforcement Discretion ............................ 23

4OA5 Other Activities ................................................................................................... 29 4OA6 Meetings, Including Exit ..................................................................................... 38

ATTACHMENT:

SUPPLEMENTARY INFORMATION

KEY POINTS OF CONTACT

.................................................................................................... A-1

LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED

..................................... A-1

LIST OF DOCUMENTS REVIEWED

........................................................................................ A-2

LIST OF ACRONYMS

............................................................................................................... A-9

Enclosure

SUMMAR Y
OF [[]]
FINDIN [[]]

GS IR 05000333/2012005; 10/01/2012 - 12/31/2012; James A. FitzPatrick Nuclear Power Plant (FitzPatrick); Follow-Up of Events.

The report covered a three-month period of inspection by resident inspectors and announced

inspections performed by regional inspectors. Inspectors identified two findings of very low safety significance (Green), which were also non-cited violations (NCVs). The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP). The cross-cutting aspects for

the findings were determined using IMC 0310, "Components Within Cross-Cutting Areas."

Findings for which the

SDP does not apply may be Green, or be assigned a severity level after
NRC management review. The
NRC 's program for overseeing the safe operation of commercial nuclear power reactors is described in
NUR [[]]

EG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.

Cornerstone: Initiating Events Green. The inspectors identified a self-revealing, Green non-cited violation (NCV) of Technical Specification (TS) 5.4, "Procedures," because FitzPatrick personnel did not perform installation of replacement reserve station service transformers (RSSTs) 71T-2 and 71T-3 in accordance with written procedures. Specifically, station personnel did not remove

the shorting bars from the current transformer (CT) circuits, as specified by the work

instructions, which impacted trip set points for the transformer differential current protection

relays. As a result, the 71T-3 differential protection circuitry actuated after the start of a

major electrical load when it was not required, which caused a transformer lockout and loss of offsite power. As immediate corrective action, operators reestablished station power from the normal station service transformer via the 345 kilovolt (KV) back feed and secured the

emergency diesel generators (EDGs). The issue was entered into the corrective action

program (CAP) as condition report (CR)-JAF-2012-06866.

The finding was more than minor because it affected the equipment performance attribute of the Initiating Events cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations.

The inspectors evaluated the finding in accordance with IMC 0609, Appendix G, "Shutdown

Operations Significance Determination Process." Per Attachment 1, "Shutdown Operations

Significance Determination Process Phase 1 Operational Checklists for both

PWR s and

BWRs," Checklist 7, "BWR Refueling Operation with RCS Level > 23'," the issue constituted a finding because, after the event, FitzPatrick did not have one operable qualified circuit

between the offsite transmission network and the onsite 1E AC electrical power distribution

subsystems. Also, per Checklist 7, this was not a finding requiring phase 2 or phase 3

analysis, nor did it constitute a loss of control event per Appendix G, Table 1. Therefore, the finding screened as very low safety significance (Green).

This finding had a cross-cutting aspect in the area of Human Performance, Resources,

because Entergy staff did not provide an accurate and up-to-date work package for

installation of the

RSST s, in that the package did not include a drawing of the

CT shorting terminal configured with the shorting bar removed, nor did they ensure that the work package was appropriately updated with clarifying information after workers questioned the

existing instructions H.2(c). (Section 4OA3)

Enclosure Cornerstone: Mitigating Systems Green. The inspectors identified a self-revealing, Green non-cited violation (NCV) of Technical Specification (TS) 5.4, "Procedures," because Entergy did not establish and implement an adequate procedure for installation of a 4160 volt alternating current (VAC) circuit breaker. Specifically, FitzPatrick's procedure for 4160 VAC circuit breaker installation did not provide sufficient guidance to station personnel to preclude physical misalignment of

the 'A' emergency diesel generator (EDG) output breaker which occurred during installation on September 15, 2011, and resulted in failure of the breaker to close when required

following a loss of offsite power on October 5, 2012. As immediate corrective action, the 'A'

EDG output breaker was racked out, re-aligned in the cubicle, and racked back in such that it was no longer misaligned and was flush with the front of the cubicle. An instrumented test of the 'A' and 'C'

EDGs was performed and all breakers operated correctly. The issue was

entered into the corrective action program (CAP) as condition report (CR)-JAF-2012-06868.

The finding was more than minor because it affected the equipment performance attribute of the Mitigating Systems cornerstone objective to ensure the reliability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the reliability of Division 1 EDG automatic operation was degraded for approximately one year due to the

'A' EDG breaker misalignment issue. Although the issue was identified while the plant was

shut down, the inspectors determined that it was appropriate to evaluate the condition in accordance with the at-power

SDP because the condition existed for the previous year. In accordance with Inspection Manual Chapter (

IMC) 0609, Appendix A, "The Significance

Determination Process (SDP) for Findings At-Power," the inspectors determined that the

finding was of very low safety significance because the finding was not a design qualification

deficiency resulting in a loss of functionality or operability, did not represent an actual loss of

safety function of a system or train of equipment, and was not potentially risk significant due to external initiating events. Specifically, the 'A' EDG breaker continued to perform its safety function as evidenced by monthly surveillance tests until the misalignment condition

ultimately impacted its ability to close subsequent to October 3, 2012 testing.

The finding had a cross-cutting aspect in the area of Human Performance, Resources, because FitzPatrick personnel did not ensure that a complete, accurate and up-to-date procedure was available for 4160 VAC circuit breaker installation. Specifically, procedure

did not include steps to ensure correct alignment during breaker racking and to verify flush

alignment H.2(c). (Section 4OA3)

Enclosure

REPORT [[]]

DETAILS Summary of Plant Status The James A. FitzPatrick Nuclear Power Plant (FitzPatrick) began the inspection period shut

down for refueling outage 20 (R20). On October 17, 2012, operators performed a reactor

startup and reached 100 percent power on October 22. On October 23, operators reduced

power to 65 percent to conduct a planned control rod pattern adjustment, and restored power to

100 percent later that day. On November 4, an uncomplicated reactor scram occurred due to an equipment problem associated with the main turbine control system. Entergy staff corrected the problem and operators performed a reactor startup on November 7. On November 9, during

power ascension with reactor power at approximately 90 percent, operators reduced power to

percent to address main condenser tube leakage conditions. Following identification and

repair, operators restored reactor power to 100 percent the following day. On November 11, an uncomplicated scram occurred due to a fire in one of the two main transformers. Following transformer replacement, operators performed a reactor startup on November 24 and reached

100 percent power on November 27. On December 2 and December 17, operators reduced

power to 75 percent to flush the main condenser water boxes due to condenser fouling. On

both occasions, operators restored reactor power to 100 percent the following day. On December 21, operators reduced power to 50 percent to address main condenser tube leakage. Following identification and repair, operators restored reactor power to 100 percent the following

day and remained at or near 100 percent power for the remainder of the inspection period.

1.

REACTO R

SAFETY Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity 1R01 Adverse Weather Protection (71111.01 - 3 samples) .1 Readiness for Seasonal Extreme Weather Conditions a. Inspection Scope The inspectors performed a review of FitzPatrick's readiness for the onset of seasonal

low temperatures. The review focused on the reactor building ventilation system, the

emergency diesel generators (EDGs), and the EDG room ventilation systems. The

inspectors reviewed the Updated Final Safety Analysis Report (UFSAR), Technical Specifications (TSs), control room logs, and the corrective action program (CAP) to determine what temperatures or other seasonal weather could challenge these systems,

and to ensure FitzPatrick personnel had adequately prepared for these challenges. The

inspectors reviewed station procedures, including FitzPatrick's seasonal weather

preparation procedure and applicable operating procedures. The inspectors performed walkdowns of the selected systems to ensure station personnel identified issues that could challenge the operability of the systems during cold weather conditions.

Documents reviewed for each section of this inspection report are listed in the

Attachment. b. Findings No findings were identified.

Enclosure .2 Readiness for Impending Extreme Weather Conditions a. Inspection Scope On October 29, 2012, the inspectors reviewed FitzPatrick's preparations for arrival of the

remnant of Hurricane Sandy. FitzPatrick operators entered AOP-13, "High Winds,

Hurricanes and Tornadoes." The inspectors verified that the actions required by this

procedure were taken and walked down the plant exterior to identify loose or inadequately protected equipment and materials. The plant did not experience any significant operational issues as a result of the storm's passage.

On November 24, 2012, the inspectors reviewed FitzPatrick's preparations for high

winds during the reactor startup from the November 11 forced outage. The inspectors walked down exterior portions of the plant to verify that materials and equipment associated with the main transformer replacement project were adequately secured.

The inspectors verified that the circulating water system was operated in accordance

with procedural requirements for high wind conditions. The plant did not experience any

significant operational issues as a result of high winds during the plant startup. b. Findings

No findings were identified. 1R04 Equipment Alignment .1 Partial System Walkdowns (71111.04Q - 4 samples) a. Inspection Scope

The inspectors performed partial walkdowns of the following systems: 'A' standby gas treatment (SGT) during 'B'

SGT maintenance on October 25, 2012 'B' main station battery following battery replacement during the refueling outage on November 1, 2012 'B'

EDG due to increased risk significance during the forced outage that followed the main transformer fire on November 15, 2012 'B' emergency service water (ESW) during 'A' ESW maintenance on December 13, 2012 The inspectors selected these systems based on their risk-significance relative to the

reactor safety cornerstones at the time they were inspected. The inspectors reviewed

applicable operating procedures, system diagrams, the

UFSAR ,

TSs, condition reports

(CRs), and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have impacted system performance of their intended safety functions. The inspectors performed field walkdowns of accessible

portions of the systems to verify system components and support equipment were aligned correctly and were operable. The inspectors examined the material condition of

the components and observed operating parameters of equipment to verify that there were no deficiencies. The inspectors also reviewed whether Entergy staff had properly

Enclosure identified equipment issues and entered them into the CAP for resolution with the appropriate significance characterization. b. Findings No findings were identified. 1R05 Fire Protection .1 Resident Inspector Quarterly Walkdowns (71111.05Q - 5 samples) a. Inspection Scope

The inspectors conducted tours of the areas listed below to assess the material

condition and operational status of fire protection features. The inspectors verified that FitzPatrick personnel controlled combustible materials and ignition sources in accordance with administrative procedures. The inspectors verified that fire protection

and suppression equipment was available for use as specified in the area pre-fire plan,

and passive fire barriers were maintained in good material condition. The inspectors

also verified that station personnel implemented compensatory measures for out of service, degraded, or inoperable fire protection equipment, as applicable, in accordance with procedures.

North

EDG spaces 272 foot elevation, fire area/zones
VI /EG-3,
EG -4,
EG -6, on November 9, 2012 Reactor building 369 foot elevation, fire area/zone
IX /
RB -1A , on December 12, 2012 'A' battery room, charger room, and corridor, fire areas/zones
III /
BR -1 and -2, and
XVI /
BR -5, on December 19, 2012 'B' battery and charger rooms, fire areas/zones
IV /
BR -3 and -4, on December 19, 2012 Cable spreading room, fire area/zone
VII /

CS-1, on December 19, 2012 b. Findings No findings were identified. .2 Fire Protection - Drill Observation (71111.05A - 1 sample) a. Inspection Scope The inspectors observed an unannounced fire brigade drill conducted on December 12, 2012, that involved a fire in the reactor water recirculation motor generator set room in the reactor building. The inspectors evaluated the readiness of the plant fire brigade to

fight fires. The inspectors verified that FitzPatrick personnel identified deficiencies,

openly discussed them in a self-critical manner at the debrief, and took appropriate

corrective actions as required. The inspectors evaluated specific attributes as follows: Proper wearing of turnout gear and self-contained breathing apparatus Proper use and layout of fire hoses Employment of appropriate fire-fighting techniques

Enclosure Sufficient fire-fighting equipment brought to the scene Effectiveness of command and control Search for victims and propagation of the fire into other plant areas Smoke removal operations Utilization of pre-planned strategies Adherence to the pre-planned drill scenario Drill objectives met The inspectors also evaluated the fire brigade's actions to determine whether these

actions were in accordance with FitzPatrick's fire-fighting strategies. b. Findings No findings were identified.

1R11 Licensed Operator Requalification Program .1 Quarterly Review of Licensed Operator Requalification Testing and Training (71111.11Q - 1 sample) a. Inspection Scope The inspectors observed licensed operator simulator training on November 13, 2012, which included a recirculating water pump trip and seal failure and a reactor feedwater

pump trip with recirculating water pump runback, and high pressure coolant injection

(HPCI) and reactor core isolation cooling (RCIC) system failures. The inspectors

evaluated operator performance during the simulated event and verified completion of risk significant operator actions, including the use of abnormal and emergency operating procedures. The inspectors assessed the clarity and effectiveness of communications,

implementation of actions in response to alarms and degrading plant conditions, and the

oversight and direction provided by the control room supervisor. Additionally, the inspectors assessed the ability of the crew and training staff to identify and document

crew performance problems. b. Findings No findings were identified. .2 Quarterly Review of Licensed Operator Performance in the Main Control Room (71111.11Q - 1 sample)

a. Inspection Scope

On October 17, 2012, the inspectors observed control room operators during the reactor startup following R20. Portions of the reactor startup, including the approach to and achievement of criticality, and heatup, were observed. The inspectors observed crew performance to verify that procedure use, crew communications, and coordination of

activities between work groups met established expectations and standards.

Enclosure b. Findings No findings were identified. 1R12 Maintenance Effectiveness (71111.12Q - 2 samples) a. Inspection Scope The inspectors reviewed the samples listed below to assess the effectiveness of maintenance activities on structure, system, or component (SSC) performance and reliability. The inspectors reviewed system health reports, CAP documents, and

maintenance rule basis documents to ensure that FitzPatrick staff was identifying and

properly evaluating performance problems within the scope of the maintenance rule. For

each sample selected, the inspectors verified that the

SSC was properly scoped into the maintenance rule in accordance with Title 10, Code of Federal Regulations (10

CFR) Part 50.65 and verified that the (a)(2) performance criteria established by FitzPatrick

staff was reasonable. For SSCs classified as (a)(1), the inspectors assessed the

adequacy of goals and corrective actions to return these SSCs to (a)(2). Additionally,

the inspectors ensured that FitzPatrick staff was identifying and addressing common cause failures that occurred within and across maintenance rule system boundaries. Analog Transmitter Trip System Neutron Monitoring b. Findings No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - 4 samples) a. Inspection Scope The inspectors reviewed maintenance activities to verify that the appropriate risk

assessments were performed prior to removing equipment for work. The inspectors reviewed whether risk assessments were performed as required by 10 CFR 50.65(a)(4), and were accurate and complete. When emergent work was performed, the inspectors

reviewed whether plant risk was promptly reassessed and managed. The inspectors

also walked down selected areas of the plant which became more risk significant

because of the maintenance activities to ensure they were appropriately controlled to

maintain the expected risk condition. The reviews focused on the following activities: Emergent charcoal replacement on 'B' SGT on October 25, 2012 Spent fuel pool cooling system protection measures due to lower time to boil following R20, with walkdowns performed during the week of October 29, 2012 Power ascension to 100 percent following the November 11 forced outage, a power reduction to 65 percent for a control rod pattern adjustment, high pressure coolant injection system quarterly surveillance test, and emergent maintenance to

troubleshoot a power supply problem with the 'B' rod block monitor during the week

of November 26, 2012 Power reduction to 75 percent to flush the main condenser water boxes due to

Enclosure fouling, 'B' residual heat removal (RHR) and RHR service water system quarterly surveillance tests, and a power reduction to 50 percent to support emergent

maintenance to identify and plug leaking main condenser tubes during the week of December 17, 2012 b. Findings No findings were identified. 1R15 Operability Determinations and Functionality Assessments (71111.15 - 3 samples) a. Inspection Scope The inspectors reviewed operability determinations for the following degraded or non-

conforming conditions:

CR -
JAF -2012-05060 and
CR -
JAF -2012-05063 concerning the effect of two thermal relief valves,
10RV -41D and 14

SV-20A, that had exceeded their required lift test frequency on operability of the associated systems, 'D' RHR and 'A' core spray, on

September 4, 2012

CR -
JAF -2011-04144 concerning control rod operability during startup due to channel bow considerations, on October 5, 2012
CR -

[[::JAF-2012-07728|JAF-2012-07728]], concerning 'F' safety relief valve (SRV) downward first stage temperature spikes that could be indicative of pilot valve leakage, making the SRV possibly susceptible to spurious operation, on October 25, 2012 The inspectors selected these issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the

operability determinations to assess whether TS operability was properly justified and

the subject component or system remained available such that no unrecognized

increase in risk occurred. The inspectors compared the operability and design criteria in

the appropriate sections of the

TS and

UFSAR to FitzPatrick personnel's evaluations to determine whether the components or systems were operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the

measures in place would function as intended and were properly controlled by

FitzPatrick personnel. The inspectors determined, where appropriate, compliance with

bounding limitations associated with the evaluations. b. Findings

No findings were identified.

Enclosure 1R18 Plant Modifications (71111.18 - 2 samples)

.1 Temporary Modifications a. Inspection Scope The inspectors reviewed temporary modification

EC 40529, "02

PT-134D Alternate Input

due to

29MST -1002D Leak." Pressure transmitter 02

PT-134D senses main steam line

pressure at the main turbine inlet, which is used as an input to the primary containment isolation system for automatic closure of the main steam isolation valves on low main steam line pressure with the reactor in the 'Run' mode. 29MST-1002D is a valve in the

2PT-134D sensing line that developed a steam leak. The purpose of the temporary

modification was to allow 29MST-1002D to be closed for repair while maintaining

2PT-134D operable by using an alternate input source. The inspectors verified that the design bases, licensing bases, and performance

capability of the affected system was not degraded by the modification. In addition, the

inspectors reviewed modification documents associated with the design change.

b. Findings

No findings were identified. .2 Permanent Modifications a. Inspection Scope The inspectors evaluated replacement of main transformer 71T-1A implemented by engineering change package EC 41007, "Main Transformer 71T-1A Replacement." The inspectors verified that the design bases, licensing bases, and performance capability of the affected systems were not degraded by the modification. In addition, the inspectors reviewed modification documents associated with the design change and the post

modification test plan. b. Findings No findings were identified. 1R19 Post-Maintenance Testing (71111.19 - 8 samples) a. Inspection Scope The inspectors reviewed the post-maintenance tests (PMTs) for the maintenance activities listed below to verify that procedures and test activities ensured system operability and functional capability. The inspectors reviewed the test procedure to

verify that the procedure adequately tested the safety functions that may have been

affected by the maintenance activity, that the acceptance criteria in the procedure was

consistent with the information in the applicable licensing basis and/or design basis documents, and that the procedure had been properly reviewed and approved. The inspectors also witnessed the test or reviewed test data to verify that the test results

adequately demonstrated restoration of the affected safety functions.

Enclosure Work Orders (WOs) 52287092, 00252161, 52288090, 00139399, 00271390, 51693751, 51693591 for work on various 'B'

RHR system components during R20, on October 1, 2012
WO 52290498 to perform preventive maintenance on the 'A' outboard main steam isolation valve (MSIV),
29AOV -86A, on October 2, 2012
WO 00212935 to replace reserve station service transformer, 71T-2, deluge system, on October 3, 2012
WO 52292007 to perform 'A'
SRV maintenance and inservice inspection during R20, on October 10, 2012
WO 52288695 to perform the reactor pressure vessel system leakage test following work performed in containment during R20, including control rod drive mechanism replacements, on October 11, 2012
WO 52290673 to perform control rod scram time testing following refueling during R20, on October 11, 2012
WO s 00152226, 00167063, 00328937 for work to correct excessive leakage from the torus purge and inert supply and isolation valves, 27

AOV-115 and -116, on October 14, 2012 WO 332252 to replace the main turbine trip solenoid valve, on November 7, 2012 b. Findings No findings were identified. 1R20 Refueling and Other Outage Activities (71111.20 - 2 samples) .1 Refueling Outage 20 (R20) a. Inspection Scope The inspectors reviewed FitzPatrick's work schedule and outage risk plan for R20, which commenced on September 16, 2012. The inspectors reviewed FitzPatrick's

implementation of outage plans and schedules to verify that risk, industry experience,

previous site-specific problems, and defense-in-depth were considered. The inspectors

observed portions of the startup process and monitored controls associated with the

following outage activities: Configuration management, including maintenance of defense-in-depth, commensurate with the outage plan for the key safety functions and compliance with the applicable

TS [[when taking equipment out of service Installation and configuration of reactor coolant pressure, level, and temperature instruments to provide accurate indication and instrument error accounting Status and configuration of electrical systems and switchyard activities to ensure that]]

TSs were met Monitoring of decay heat removal operations Impact of outage work on the ability of the operators to operate the spent fuel pool cooling system Reactor water inventory controls, including flow paths, configurations, alternative means for inventory additions, and controls to prevent inventory loss Activities that could affect reactivity

Enclosure Maintenance of secondary containment as required by TSs Refueling activities, including fuel handling and full core verification Fatigue management Containment closeout inspection Identification and resolution of problems related to refueling outage activities These activities completed one sample, which was begun last quarter when R20 commenced. b. Findings

No findings were identified. .2 November 11, 2012, Forced Outage a. Inspection Scope On November 11, 2012, the reactor automatically scrammed from approximately 100 percent power due to a failure of main transformer 71T-1A which resulted in a main generator load rejection and turbine trip. Following repair and replacement activities, the

reactor was taken critical on November 24, 2012, and placed online on November 25,

2012. The inspectors reviewed FitzPatrick staff's implementation of forced outage plans

and schedules to verify that risk, industry experience, previous site-specific problems, and defense-in-depth were considered. The inspectors observed portions of the cooldown, heatup, and startup processes, and monitored controls associated with the following outage activities: Configuration management, including maintenance of defense-in-depth, commensurate with the outage plan for the key safety functions and compliance with the applicable

TS - 5 samples) a. Inspection Scope The inspectors observed the performance of surveillance tests (]]

STs) and/or reviewed test data of selected risk-significant SSCs to assess whether test results satisfied

technical specifications, the

UFS [[]]

AR, and station procedure requirements. The

inspectors verified that test acceptance criteria were clear, tests demonstrated

operational readiness and were consistent with design documentation, test

Enclosure instrumentation had current calibrations and the appropriate range and accuracy for the application, tests were performed as written, and applicable test prerequisites were

satisfied. Upon test completion, the inspectors considered whether the test results supported that equipment was capable of performing the required safety functions. The inspectors reviewed the following

ST s:
ST -9CB, "EDG B and D Load Sequencing Test and
4KV Emergency Power System Voltage Relays Instrument Functional Test," on October 2, 2012
ST -9NB, "EDG Subsystem B Logic System Functional Test," on October 2, 2012
ST -9
CA , "EDG A and C Load Sequencing Test and
4KV Emergency Power System Voltage Relays Instrument Functional Test," on October 3, 2012
MST -071.26, "Station Battery A Modified Performance Test," on October 4, 2012
ST -3

PA, "'A' Core Spray Quarterly Operability (IST)," November 9, 2012 b. Findings No findings were identified.

2.

RADIAT [[]]
ION [[]]
SAFETY Cornerstones: Occupational Radiation Safety and Public Radiation Safety 2

RS1 Radiological Hazard Assessment and Exposure Controls (71124.01 - 1 sample) During the week of September 24 through 28, 2012, the inspectors reviewed and assessed FitzPatrick staff's performance in assessing the radiological hazards and exposure control in the workplace. The inspectors used the requirements in 10 CFR

Part 20 and guidance in Regulatory Guide (RG) 8.38, "Control of Access to High and

Very High Radiation Areas for Nuclear Plants," the

TS s, and the Entergy's procedures required by

TSs as criteria for determining compliance. a. Inspection Scope Inspection Planning The inspectors reviewed FitzPatrick's 2012 performance indicators for the occupational exposure cornerstone for FitzPatrick. The inspectors reviewed the results of radiation

protection (RP) program audits. The inspectors reviewed any reports of operational

occurrences related to occupational radiation safety since the last inspection. Radiological Hazard Assessment The inspectors reviewed whether there had been changes to plant operations since the last inspection that may result in a significant new radiological hazard for onsite workers or members of the public. The inspectors evaluated whether FitzPatrick staff assessed

the potential impact of these changes and had implemented periodic monitoring, as

appropriate, to detect and quantify the radiological hazard. The inspectors reviewed the last two radiological surveys from the drywell, reactor building, and 'A' reactor water cleanup pump. The inspectors evaluated whether the

Enclosure thoroughness and frequency of the surveys were appropriate for the given new radiological hazard. The inspectors conducted walkdowns and independent radiation measurements in the facility, including radioactive waste processing, storage, and handling areas to evaluate material and radiological conditions. The inspectors selected the following risk-significant work activities that involved exposure to radiation. In-service inspection (ISI) inside the drywell Reactor disassembly/reassembly Safety relief valve work For these work activities, the inspectors assessed whether the pre-work surveys

performed were appropriate to identify and quantify the radiological hazard and to

establish adequate protective measures. The inspectors evaluated the radiological survey program to determine if radiological hazards were properly identified (e.g., discrete radioactive hot particles, transuranics and hard to detect nuclides in air

samples, transient dose rates and large gradients in radiation dose rates). The inspectors did not observe work in potential airborne areas as there were no posted airborne radioactivity areas during the inspection period. The inspectors evaluated

whether continuous air monitors (CAMs) were located in areas with low background radiation to minimize false alarms and were representative of actual work areas. The inspectors evaluated FitzPatrick's program for monitoring levels of loose surface

contamination in areas of the plant with the potential for the contamination to become airborne. Instructions to Workers The inspectors selected three containers holding non-exempt licensed radioactive materials that may cause unplanned or inadvertent exposure of workers. The inspectors

assessed whether the containers were labeled and controlled in accordance with 10

CFR Part 20 requirements. The inspectors reviewed the following radiation work permits (
RWP s) used to access high radiation areas (HRAs) and evaluated if the specified work control instructions and control barriers were consistent with
TS requirements for

HRAs. 20120512, ISI inside the drywell 20120701, reactor disassembly/reassembly 20120515, safety relief valve work

For these

RWP s, the inspectors assessed whether allowable stay times or permissible dose for radiologically significant work under each

RWP were clearly identified. The inspectors evaluated whether Electronic Personal Dosimeter (EPD) alarm set-points were in conformance with survey indications and plant procedural requirements.

Enclosure For work activities that could suddenly and severely increase radiological conditions, the inspectors assessed FitzPatrick's means to inform workers of these changes that could

significantly impact their occupational dose. Contamination and Radioactive Material Control The inspectors observed the control point access/egress where FitzPatrick staff monitored potentially contaminated material leaving the radiological control area and

inspected the methods used for control, survey, and release of these materials from

these areas. The inspectors observed the performance of personnel surveying and releasing material for unrestricted use and evaluated whether the work was performed in accordance with plant procedures. The inspectors assessed whether the radiation monitoring instrumentation used for equipment release and personnel contamination

surveys had appropriate sensitivity for the type(s) of radiation present. The inspectors reviewed FitzPatrick staff's criteria for the survey and release of potentially contaminated material. The inspectors evaluated whether there was guidance on how to respond to alarms that indicate the presence of licensed radioactive material. The inspectors reviewed FitzPatrick's procedures and records to verify that the radiation detection instrumentation was used at its typical sensitivity level based on appropriate counting parameters. The inspectors selected two sealed sources from FitzPatrick's inventory records and assessed whether the sources were accounted for and were

tested for loose surface contamination. The inspectors evaluated whether any recent transactions involving nationally tracked sources were reported in accordance with10 CFR Part 20 requirements. Radiological Hazards Control and Work Coverage The inspectors evaluated ambient radiological conditions and performed independent radiation measurements during walkdowns of the facility. The inspectors assessed

whether the conditions were consistent with applicable posted surveys, RWPs, and

associated worker briefings. The inspectors evaluated the adequacy of radiological controls, such as required surveys, radiation protection job coverage and contamination controls. The inspectors evaluated FitzPatrick staff's use of

EPD s in high noise areas that were also

HRAs or

Locked High Radiation Areas (LHRAs). The inspectors assessed whether radiation monitoring devices were placed on the individual's body consistent with FitzPatrick's procedures. The inspectors assessed

whether the dosimeter was placed in the location of highest expected dose or that FitzPatrick staff properly implemented an NRC-approved method of determining effective dose equivalent. The inspectors reviewed the application of dosimetry to effectively monitor exposure to personnel in high-radiation work areas with significant dose rate gradients.

Enclosure The inspectors did not review any RWPs for work within airborne radioactivity areas with the potential for individual worker internal exposures as no airborne radioactivity areas

were present during the inspection period. The inspectors examined FitzPatrick's physical and programmatic controls for highly activated or contaminated materials stored within spent fuel and other storage pools at

FitzPatrick. The inspectors assessed whether appropriate controls were in place to

preclude inadvertent removal of these materials from the pool. The inspectors examined the posting and physical controls for selected

HRA s,
LHRA s and very high radiation areas (VHRAs) to verify conformance with the occupational performance indicator. Risk-Significant
HRA and
VHRA Controls The inspectors discussed with first-line health physics supervisors the controls in place for special areas that have the potential to become
VH [[]]

RAs during certain plant

operations. The inspectors assessed whether these plant operations require communication beforehand with the health physics group, so as to allow corresponding timely actions to properly post, control, and monitor the radiation hazards including re-

access authorization. Radiation Worker The inspectors observed the performance of radiation workers with respect to stated

RP work requirements. The inspectors assessed whether workers were aware of the radiological conditions in their workplace and the

RWP controls/limits in place, and

whether their behavior reflected the level of radiological hazards present.

RP Technician Proficiency The inspectors observed the performance of the

RP technicians with respect to controlling radiation work. The inspectors evaluated whether technicians were aware of the radiological conditions in their workplace and the RWP controls/limits, and whether their behavior was consistent with their training and qualifications with respect to the

radiological hazards and work activities. Problem Identification and Resolution The inspectors evaluated whether problems associated with radiation monitoring and exposure control were being identified by FitzPatrick staff at an appropriate threshold and were properly addressed for resolution in the licensee's CAP. The inspectors

assessed the appropriateness of the corrective actions for a selected sample of

problems documented by FitzPatrick staff that involve radiation monitoring and exposure controls. The inspectors assessed FitzPatrick staff's process for applying operating

experience to their plant. b. Findings No findings were identified.

Enclosure

2RS 2 Occupational
ALARA Planning and Controls (71124.02) The inspectors assessed performance with respect to maintaining occupational individual and collective radiation exposures as low as is reasonably achievable (ALARA). The inspectors used the requirements in
10 CFR Part 20,

RG 8.8,

"Information Relevant to Ensuring that Occupational Radiation Exposures at Nuclear Power Plants will be As Low As Reasonably Achievable," RG 8.10, "Operating

Philosophy for Maintaining Occupational Radiation Exposure As Low as Reasonably Achievable," the

TS s, and FitzPatrick's procedures required by

TSs as criteria for determining compliance. a. Inspection Scope Inspection Planning The inspectors reviewed pertinent information regarding FitzPatrick's collective dose history, current exposure trends, and ongoing or planned activities in order to assess

current performance and exposure challenges. The inspectors reviewed the plant's

three year rolling average collective exposure. The inspectors compared the site-specific trends in collective exposures against the industry average values and those values from similar vintage reactors. In addition, the inspectors reviewed any changes in the radioactive source term by reviewing the trend

in average contact dose rate with recirculation piping. The inspectors reviewed site-

specific procedures associated with maintaining occupational exposures

ALA [[]]

RA, which

included a review of processes used to estimate and track exposures from specific work

activities. Radiological Work Planning The inspectors selected the following work activities that had the highest exposure significance. 20120512,

ISI inside the drywell 20120701, reactor disassembly/reassembly 20120515, safety relief valve work The inspectors reviewed the

ALARA work activity evaluations, exposure estimates, and exposure reduction requirements. The inspectors determined whether FitzPatrick staff

reasonably grouped the radiological work into work activities, based on historical

precedence, industry norms, and/or special circumstances. The inspectors assessed whether FitzPatrick staff's planning identified appropriate dose reduction techniques, considered alternate dose reduction features, and estimated reasonable dose goals. The inspectors evaluated whether FitzPatrick staff's

ALA [[]]

RA

assessment had taken into account decreased worker efficiency from use of respiratory

protective devices and/or heat stress mitigation equipment. The inspectors determined

whether FitzPatrick staff's work planning considered the use of remote technologies as a means to reduce dose and the use of dose reduction insights from industry operating experience and plant-specific lessons learned. The inspectors assessed the integration

of

ALARA requirements into work procedure and

RWP documents.

Enclosure Verification of Dose Estimates and Exposure Tracking Systems The inspectors reviewed the assumptions and basis for the current annual collective dose estimate for accuracy. The inspectors reviewed applicable procedures to determine the methodology for estimating exposures from specific work activities and for department and station collective dose goals. The inspectors evaluated whether FitzPatrick staff had established measures to track, trend, and if necessary, to reduce occupational doses for ongoing work activities. The

inspectors assessed whether dose threshold criteria were established to prompt additional reviews and/or additional

ALA [[]]

RA planning and controls. The inspectors evaluated FitzPatrick staff's method of adjusting exposure estimates, or re-planning work, when unexpected changes in scope or emergent work were

encountered. The inspectors assessed whether adjustments to exposure estimates were

based on sound

RP and

ALARA principles or if they were just adjusted to account for failures to plan/control the work. Source Term Reduction and Control The inspectors used FitzPatrick's records to determine the historical trends and current status of plant source term known to contribute to elevated facility collective dose. The inspectors assessed whether FitzPatrick staff had made allowances or developed contingency plans for expected changes in the source term as the result of changes in

plant fuel performance issues or changes in plant primary chemistry. Radiation Worker Performance The inspectors observed radiation worker and

RP technician performance during work activities being performed in radiation areas and
HRA s. The inspectors evaluated whether workers demonstrated the
ALARA philosophy in practice and whether there were any procedure or
RWP compliance issues. Problem Identification and Resolution The inspectors evaluated whether problems associated with
ALARA planning and controls are being identified by FitzPatrick staff at an appropriate threshold and were properly addressed for resolution in FitzPatrick's

CAP. The inspectors assessed FitzPatrick's process for applying operating experience to their plant.

b. Findings No findings were identified. 2RS3 In-Plant Airborne Radioactivity Control and Mitigation (71124.03) The inspectors verified in-plant airborne concentrations were being controlled consistent

with

ALARA principles and the use of respiratory protection devices on-site did not pose an undue risk to the wearer. The inspectors used the requirements in 10
CFR Part 20, the guidance in
RG 8.15, "Acceptable Programs for Respiratory Protection,"

RG 8.25,

Enclosure "Air Sampling in the Workplace,"

NUREG -0041, "Manual of Respiratory Protection Against Airborne Radioactive Material," the

TSs, and FitzPatrick's procedures required

by

TS s as criteria for determining compliance. a. Inspection Scope The inspectors reviewed FitzPatrick's

UFSAR to identify areas of the plant designed as

potential airborne radiation areas and any associated ventilation systems or airborne monitoring instrumentation. This review included instruments used to identify changing airborne radiological conditions such that actions to prevent an internal uptake may be taken. The inspectors reviewed reported performance indicators to identify any related

to unintended dose resulting from intakes of radioactive material. Engineering Controls The inspectors reviewed FitzPatrick staff's use of permanent and temporary ventilation to determine whether the licensee used ventilation systems as part of its engineering controls to control airborne radioactivity. The inspectors reviewed procedural guidance

for use of installed plant systems to reduce dose and assessed whether the systems were used, to the extent practicable, during high-risk activities. The inspectors selected the reactor building and the

SGT [[system as installed ventilation systems used to mitigate the potential for airborne radioactivity. The inspectors evaluated whether the ventilation system operating parameters, were consistent with maintaining concentrations of airborne radioactivity in work areas below the concentrations of an airborne radioactive material area. The inspectors selected the drywell temporary ventilation system setup used to support work in contaminated areas. The inspectors assessed whether the use of the system was consistent with FitzPatrick's procedural guidance and]]

ALARA concept. The inspectors assessed whether FitzPatrick staff had established threshold criteria for evaluating levels of airborne beta-emitting and alpha-emitting radionuclides.

b. Findings No findings were identified. 4.

OTHER [[]]

ACTIVITIES

4OA1 Performance Indicator Verification (71151)

.1 Mitigating Systems Performance Index (5 samples) a. Inspection Scope The inspectors reviewed FitzPatrick staff's submittal of the Mitigating Systems

Performance Index (MSPI) for the following systems for the period of October 1, 2011 through September 30, 2012.

Enclosure

MSPI , emergency alternating current power system
MSPI , high pressure injection system
MSPI , heat removal system
MSPI , residual heat removal system
MSPI , cooling water systems To determine the accuracy of the performance indicator (

PI) data reported during this period, the inspectors used definitions and guidance contained in Nuclear Energy

Institute (NEI) Document 99-02, "Regulatory Assessment Performance Indicator

Guideline," Revision 6, and discussed specific questions with the

HP [[]]

CI system engineer.

The inspectors also reviewed station operator narrative logs,

MS [[]]

PI/World Association of

Nuclear Operators (WANO)

PI data sheets,

EDG demand logs, a learning organization report (LO-HQNLO-2007-00076), and NRC integrated inspection reports to validate the accuracy of the submittals.

b. Findings No findings were identified.

.2 Occupational Exposure Control Effectiveness (1 sample) a. Inspection Scope During the week of September 24 through 28, 2012, the inspectors sampled FitzPatrick submittals for the occupational radiological occurrences

PI for the period from the fourth quarter 2011 through third quarter 2012. The inspectors used

PI definitions and guidance contained in the NEI 99-02, "Regulatory Assessment Performance Indicator

Guideline," Revision 6, to determine the accuracy of the

PI data reported during this period. The inspectors reviewed FitzPatrick staff's assessment of the
PI for occupational radiation safety to determine if the related data was adequately assessed and reported. To assess the adequacy of FitzPatrick's
PI data collection and analyses, the inspectors discussed with

RP staff the scope and breadth of its data review and the results of those

reviews. The inspectors independently reviewed electronic personal dosimetry accumulated dose alarms, dose reports, and dose assignments for any intakes that occurred during the time period reviewed to determine if there were potentially

unrecognized PI occurrences. The inspectors also conducted walkdowns of numerous

locked high and very high radiation area entrances to determine the adequacy of the

controls in place for these areas.

b. Findings No findings were identified.

Enclosure

4OA [[2 Problem Identification and Resolution (71152 - 2 samples) .1 Routine Review of Problem Identification and Resolution Activities a. Inspection Scope As required by Inspection Procedure 71152, "Problem Identification and Resolution," the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that FitzPatrick staff entered issues into the]]

CAP at an

appropriate threshold, gave adequate attention to timely corrective actions, and

identified and addressed adverse trends. In order to assist with the identification of

repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the

CAP and periodically attended

CR screening meetings.

b. Findings No findings were identified.

.2 Semi-Annual Trend Review (1 sample) a. Inspection Scope The inspectors performed a semi-annual review of site issues, as required by Inspection

Procedure 71152, "Problem Identification and Resolution," to identify trends that might

indicate the existence of more significant safety issues. In this review, the inspectors

included repetitive or closely-related issues that may have been documented by

FitzPatrick personnel outside of the

CAP , such as trend reports,
PI s, major equipment problem lists, system health reports, maintenance rule assessments, and the
CAP backlog. The inspectors also reviewed FitzPatrick's

CAP database for the third and

fourth quarters of 2012 to assess CRs written in various subject areas (equipment

problems, human performance issues, etc.), as well as individual issues identified during the

NRC 's daily
CR review (Section
4OA 2.1). The inspectors reviewed the FitzPatrick quarterly trend report for the second quarter of 2012, conducted under

EN-LI-121, "Entergy Trending Process," to verify that FitzPatrick personnel were appropriately

evaluating and trending adverse conditions in accordance with applicable procedures.

b. Findings and Observations No findings were identified. The inspectors evaluated a sample of CRs generated over the course of the past two

quarters by departments that provide input to the quarterly trend reports. The inspectors determined that, in most cases, the issues were appropriately evaluated by Entergy staff for potential trends and resolved within the scope of the corrective action program.

However, the inspectors noted instances where issue trending had not been utilized and

may have proven useful. For example, there were multiple instances of emergency

warning siren malfunctions during the past six months, most associated with siren #4. Although the individual issues were addressed through the CAP, the inspectors did not initially see an indication that they had collectively been evaluated to determine if an

adverse trend existed. Following discussions regarding the number of siren failures,

Enclosure FitzPatrick staff initiated

CR -

[[::JAF-2012-8040|JAF-2012-8040]] to evaluate the potential adverse trend. Although the individual issues were being addressed, the inspectors considered that this

particular issue satisfied the

EN -

LI-121 definition of an adverse trend. While this was not a violation of regulatory requirements, the inspectors determined it was a missed opportunity to effectively use all of the tools available in the CAP.

.3 Annual Sample: Review of the Operator Workaround Program (1 sample) a. Inspection Scope The inspectors reviewed the cumulative effects of the existing operator workarounds,

operator burdens, operator aids and disabled alarms, and open main control room

deficiencies to identify any effect on emergency operating procedure operator actions,

and any impact on possible initiating events and mitigating systems. The inspectors evaluated whether station personnel had identified, assessed, and reviewed operator workarounds as specified in Entergy Fleet procedure

EN -

FAP-OP-006, "Operator

Aggregate Impact Index Performance Indicator."

The inspectors reviewed FitzPatrick's process to identify, prioritize and resolve main control room distractions to minimize operator burdens. The inspectors reviewed the system used to track these operator workarounds and recent FitzPatrick staff

evaluations of the aggregate impact index. The inspectors also routinely tour the control

room and discuss operator workarounds with the operators to ensure the items are

addressed on a schedule consistent with their relative safety significance. b. Findings and Observations No findings were identified.

The inspectors determined that the issues reviewed did not adversely affect the capability of the operators to implement abnormal or emergency operating procedures. The inspectors also verified that FitzPatrick staff entered operator workarounds and

burdens into the corrective action program at an appropriate threshold and planned or

implemented corrective actions commensurate with their safety significance.

4OA system and]]

RHR shutdown cooling secured. The new reserve

station service transformers (RSSTs) had just been placed in service and were providing

site power. Preparations were in progress for installation of the fuel pool gates to

support cavity drain down and reactor reassembly.

At 1:01 pm, operators started the 'A' core spray pump to support testing. Immediately thereafter, a loss of offsite power occurred due to a lockout of the

RS [[]]

STs. Operators

also received a reactor scram (all rods were already fully inserted), and the 'A' core

Enclosure spray pump shut down. All four

EDG s automatically started and all closed in to reenergize their respective safety busses, with the exception of the 'A'

EDG, which

started but did not close in. The inspectors responded to the control room to monitor plant response and observe

operator activities. The inspectors verified that operators responded in accordance with

the applicable emergency and abnormal operating procedures. The inspectors

confirmed that the station's response was consistent with the requirements of the site

emergency plan, and that the event was reported to the

NRC as required by 10

CFR Part 50.72.

b. Findings

(1) Failure to Install Reserve Station Service Transformers in Accordance with Procedure Introduction. The inspectors identified a self-revealing, Green non-cited violation (NCV) of TS 5.4, "Procedures," because station personnel did not perform installation of the

replacement

RS [[]]

STs, 71T-2 and 71T-3, in accordance with written procedures.

Specifically, station personnel did not remove the shorting bars from the current transformer (CT) circuits, as specified by the work instructions, which impacted trip set points for the transformer differential current protection relays. Description. FitzPatrick station receives offsite electrical power from two

115 KV supply lines, lines 3 and 4, which are stepped down to 4160 volts through the

RSSTs, 71T-2

and 71T-3. These provide station power when the plant is shut down and when the main generator is off line. During plant operation, station electrical loads are supplied by normal station service transformer (NSST) 71T-4, which takes power from the main

generator output. In the event that neither of these sources is available, two pair of

EDG s automatically start to supply safety class electrical loads; 'A' and 'C'

EDGs supply

Division 1 loads through Bus 10500, and 'B' and 'D'

EDG s supply Division 2 loads through Bus 10600. During the
RSST replacement, power was fed back through the main transformers from the normal outgoing
345 KV transmission system to provide station power through the
NSST. The
RSST s were replaced during R20 under Engineering Change (

EC) 12703, "Replace

Reserve Station Service Transformers," which had been prepared by a contract organization. The installations were performed by contract electricians with management and oversight provided by the transformer vendor and Entergy project managers.

Enclosure The

RSST s are provided with fault protection, in part, using a phase differential current protection scheme. Phase currents are sensed using current transformers (

CTs), which

provide reduced values of current to the protection circuit relays and other components.

CT connections are made to the protective circuitry on a shorting terminal block in the

RSST control panel. A conducting (shorting) bar is mounted above the shorting terminal

block, which allows individual termination points on the shorting terminal block to be

shorted by installation of screws through the shorting bar. The as-sent configuration of

the new transformers had these shorting screws installed, and the EC preparers realized

that they needed to be removed during installation of the

RSST s. Rather than specifying the standard practice of removing the shorting screws, the

EC preparers instructed removal of the shorting bar itself. However, this action would result in a different

terminal configuration than was shown in the applicable EC circuit drawing, which had

not been modified to reflect the shorting bar removal and still showed the as-sent

configuration. The vendor project manager considered that the statement to remove the shorting bar

was an administrative error, and that the intent of the step was to remove the shorting

screws for the CTs that would be placed in service. Based on this interpretation, he

consulted the Entergy responsible engineer to verify which screws needed to be removed. Based on the as-sent circuit drawing in the EC, they concluded that two of the three shorting screws should remain installed. 71T-2 and 71T-3 were returned to service on October 5, 2012. At that point in the

refueling outage, site electrical requirements were so limited that the transformer

differential protection circuitry did not initially actuate, despite the incorrect CT setup. However, when operators started the 'A' core spray pump to support unrelated testing, the 71T-3 phase A differential protection relay tripped and produced a lockout of both

71T-3 and 71T-2. The EDGs automatically started and reenergized the 10500 and

10600 Busses. The loss of offsite power did not cause a loss of core or fuel pool cooling because the refueling cavity was flooded, the fuel pool gates were removed, and the decay heat

removal (DHR) system was in service. The DHR system is an alternate heat removal

system that was designed to allow RHR shutdown cooling to be secured during refueling

outages. System operation was not interrupted because it is powered from a different

offsite circuit. Nonetheless, the loss of offsite power significantly impacted the plant risk profile, which previously had been Green for all shutdown safety functions As immediate corrective action, operators reestablished station power from the

NSST via the 345
KV back feed and secured the
EDG s. The issue was entered into the
CAP as
CR -
JAF -2012-06866. Troubleshooting identified the
CT shorting bars had not been removed during installation of either
RSST. Analysis. The inspectors determined that the failure of station personnel to remove the
CT shorting bars as specified by the

EC 12703 work instructions was a performance

deficiency that was reasonably within Entergy staff's ability to foresee and correct. The

finding was more than minor because it affected the equipment performance attribute of the Initiating Events cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power

operations. The finding also was similar to example 4.b in Inspection Manual Chapter

(IMC) 0612, Appendix E, "Examples of Minor Issues," in that the error caused a

Enclosure transient. The inspectors evaluated the finding in accordance with IMC 0609, Appendix G, "Shutdown Operations Significance Determination Process." Per Attachment 1,

"Shutdown Operations Significance Determination Process Phase 1 Operational Checklists for both

PWR s and

BWRs," Checklist 7, "BWR Refueling Operation with RCS Level > 23'," the issue constituted a finding because, after the event, FitzPatrick did not

have one operable qualified circuit between the offsite transmission network and the

onsite 1E AC electrical power distribution subsystems. Also per Checklist 7, this was not a finding requiring phase 2 or phase 3 analysis, nor did it constitute a loss of control

event per Appendix G, Table 1. Therefore, the finding screened as very low safety significance (Green). This finding had a cross-cutting aspect in the area of Human Performance, Resources,

because Entergy staff did not provide an accurate and up-to-date work package for

installation of the

RSST s, in that the package did not include a drawing of the

CT shorting terminal configured with the shorting bar removed, nor did they ensure that the work package was appropriately updated with clarifying information after workers

questioned the existing instructions H.2(c). Enforcement.

TS 5.4, "Procedures," states, in part, "Written procedures shall be established, implemented, and maintained covering . . . the applicable procedures recommended in

RG 1.33, Appendix A, November 1972." RG 1.33, Appendix A,

November 1972,Section I, "Procedures for Performing Maintenance," states, in part,

"Maintenance which can affect the performance of safety-related equipment should be

properly preplanned and performed in accordance with written procedures . . ." RG

1.33, Appendix A, November 1972, Section D, Procedures for Startup, Operation, and Shutdown of Safety Related BWR Systems," includes the offsite electrical system as such a system. Contrary to the above, during the 2012 FitzPatrick refueling outage, maintenance which

could affect the performance of the offsite electrical system, specifically, replacement of

RSST s 71T-2 and 71T-3, was not properly implemented by station personnel in accordance with written procedures, in that the

CT shorting bars were not removed as

specified by the EC 12703 work instructions. As a result, on October 5, 2012, the 71T-3

phase A differential protection relay tripped in response to the start of the 'A' core spray

pump and produced a lockout of both

RS [[]]

STs and a loss of offsite power. Because this

issue was of very low safety significance (Green) and Entergy entered it into their corrective action program as

CR -
JAF -2012-06866, this finding is being treated as an
NCV , consistent with the
NRC Enforcement Policy. (NCV 05000333/2012005-01, Failure to Install Reserve Station Service Transformers in Accordance with Procedure). (2) Failure of 'A'
EDG Output Breaker to Close Following Loss of Offsite Power Introduction. The inspectors identified a self-revealing, Green

NCV of TS 5.4, "Procedures," because Entergy did not establish and implement an adequate procedure

for installation of a 4160 volt alternating current (VAC) circuit breaker such that the

breaker was aligned properly upon installation. Specifically, FitzPatrick's procedure for

4160 VAC circuit breaker installation did not provide sufficient guidance to station personnel to preclude misalignment of the 'A'

EDG output breaker which occurred during

installation on September 15, 2011.

Enclosure Description. At 1:01 pm on October 5, 2012, a loss of offsite power occurred at FitzPatrick. The four

EDG s automatically started; however, the 'A'
EDG output breaker did not close as expected. Its companion Division
1 EDG ('C'

EDG) operated as expected to reenergize the 10500 Bus. Entergy's troubleshooting revealed that the 'A' EDG output breaker, 71-10502, was not properly aligned in its cubicle and thereby

prevented the normal Division I EDG starting sequence from being completed as

expected. Subsequent to the event, Entergy staff identified the top edge of the breaker

was not flush with the cubicle, but rather, protruded outward; and the breaker was not

centered in the cubicle, being flush on one side with a gap on the other, as opposed to having equal gaps on both sides.

FitzPatrick staff identified that the breaker had last been installed on September 15,

2011 when the misalignment occurred. Station personnel determined that the 'A' EDG

output breaker operated normally for approximately 12 months despite the misalignment, as supported by proper breaker operation during monthly EDG surveillance testing. However, as evidenced by the loss of offsite power event on October 5, 2012, the 'A'

EDG output breaker auxiliary contacts apparently had become disengaged due to

operationally induced vibration after the last successful operation on October 3, 2012.

The 'A'

EDG output breaker auxiliary contacts being disengaged resulted in the 'A-C'
EDG tie breaker not closing during the normal Division
EDG starting sequence, thereby permitting only one
EDG to energize the 10500 Bus. The inspectors determined that procedure
OP -46A, "4160 V and 600 V Normal

AC

Power Distribution," did not include steps to ensure correct alignment during breaker

racking and to verify flush alignment in the breaker cubicle following racking. The inspectors also determined that the Division I EDG remained operable but degraded until the October 3, 2012 surveillance run after which the auxiliary contacts apparently

became disengaged. The inspectors also noted that, given the operational condition at

that time, (refueling), the Division I

EDG function was not required by

TS from October 2

until October 5 when the problem revealed itself. The issue was entered into the corrective action program as

CR -

[[::JAF-2012-06868|JAF-2012-06868]].

Entergy staff corrected the misalignment of the 'A' EDG output breaker and conducted

an instrumented run of the 'A' and 'C'

EDG s to verify Division I

EDG breakers operated

correctly. FitzPatrick staff initiated a change to procedure OP-46A, "4160 V and 600 V

Normal

AC [[Power Distribution," to include steps to ensure correct alignment during breaker racking and flush alignment in the breaker cubicle following racking. Analysis. The inspectors determined that the failure of Entergy staff to provide an adequate procedure for installation of a 4160]]

VAC circuit breaker was a performance

deficiency that was reasonably within Entergy staff's ability to foresee and correct. The finding was more than minor because it affected the equipment performance attribute of the Mitigating Systems cornerstone objective to ensure the reliability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the

reliability of Division 1 EDG automatic operation was degraded for approximately one

year due to the 'A' EDG breaker misalignment issue. Although the issue was identified

while the plant was shut down, the inspectors determined that it was appropriate to evaluate the condition in accordance with the at-power

SDP , because the condition had existed for the previous year. In accordance with

IMC 0609, Appendix A, "The

Significance Determination Process (SDP) for Findings At-Power," the inspectors

determined that the finding was of very low safety significance (Green) because the

Enclosure finding was not a design qualification deficiency resulting in a loss of functionality or operability, did not represent an actual loss of safety function of a system or train of

equipment, and was not potentially risk significant due to external initiating events. The finding had a cross-cutting aspect in the area of Human Performance, Resources,

because FitzPatrick personnel did not ensure that a complete, accurate and up-to-date

procedure was available for 4160 VAC circuit breaker installation. Specifically,

procedure did not include steps to ensure correct alignment during breaker racking and

to verify flush alignment H.2(c). Enforcement. TS 5.4, "Procedures," states, in part, "Written procedures shall be established, implemented, and maintained covering . . . the applicable procedures

recommended in RG 1.33, Appendix A." Section I of Appendix A, "Procedures for

Performing Maintenance," states, in part, "Maintenance which can affect the performance of safety-related equipment should be properly preplanned and performed in accordance with written procedures. . ." Appendix A, Section D, "Procedures for

Startup, Operation, and Shutdown of Safety Related BWR Systems," includes

emergency power sources (e.g., diesel generator, batteries) as such a system. Contrary to the above, on September 15, 2011, maintenance which could affect the performance of the emergency diesel generators, specifically, installation of 'A' EDG

output circuit breaker 71-10502, was not properly performed, in that the written

procedure did not include steps to ensure correct alignment during breaker racking and

flush alignment in the breaker cubicle following racking. As a result, the circuit breaker

was not properly aligned such that subsequent stationary auxiliary contact disengagement resulted in failure of the breaker to automatically close when required on October 5, 2012. Because this issue was of very low safety significance (Green) and

Entergy entered it into their corrective action program as

CR -

[[::JAF-2012-06868|JAF-2012-06868]], this

finding is being treated as an

NCV , consistent with the

NRC Enforcement Policy. (NCV 05000333/2012005-02, Failure of 'A' EDG Output Breaker to Close Following Loss of Offsite Power) .2 November 4, 2012, Reactor Scram a. Inspection Scope On November 5, 2012, FitzPatrick was operating at approximately 100 percent power. At 9:41 pm, operators commenced main turbine testing in accordance with procedure

ST-21F, "Main Turbine Overspeed Trip Device and Mechanical Trip Valve Test." At 9:53

pm, an unexpected turbine trip and resultant reactor scram occurred. All control rods

inserted, as expected. The inspectors subsequently responded to the control room to monitor plant response

and observe operator activities. The inspectors verified that operator response was

consistent with the requirements of the site emergency plan and emergency and

operating procedures and operators properly reported the event in accordance with 10

CFR Parts 50.72 and 50.73. The inspectors also observed FitzPatrick staff's follow up actions related to the scram to ensure Entergy personnel implemented corrective actions commensurate with their safety significance before commencing the reactor startup.

Enclosure On November 7, 2012, the inspectors observed portions of the reactor startup, including the approach to and achievement of criticality at 3:56 am. The inspectors observed

operator performance to verify that the startup was performed in accordance with TSs and approved procedures. b. Findings No findings were identified.

.3 November 11, 2012, Reactor Scram and Notification of Unusual Event a. Inspection Scope At 3:55 a.m. on November 11, 2012, while operating at 100 percent power, a main turbine trip occurred which caused an automatic reactor scram. All systems responded as expected and operators stabilized plant conditions. Operators determined that the

turbine trip was in response to a fire in one of two main transformers. On-site fire

brigade personnel responded to combat the fire and assistance was requested from a

local fire department. At 5:45 a.m., the Shift Manager declared a discretionary Unusual Event (emergency action level HU6.1) due to the continuing fire. Site fire brigade and local fire department personnel succeeded in extinguishing the fire at 6:32 a.m., and the

licensee exited the UE at 8:01 a.m. The inspectors responded to the site, inspected the location of the fire, evaluated station response to the fire and the plant trip, and determined the plant was in a safe, stable condition. The inspectors verified that operators responded in accordance with the

applicable emergency and abnormal operating procedures. The inspectors confirmed

that the station's response was consistent with the requirements of the site emergency

plan, and that the event was reported to the

NRC as required by 10
CFR Part 50.72. b. Findings No findings were identified.
4OA 5 Other Activities .1 License Renewal Activities (
IP 71003) a. Inspection Scope This inspection was performed by
NRC Region I based inspectors to evaluate the license renewal activities at FitzPatrick in accordance with

IP 71003. The inspectors performed in-plant observations of license renewal related activities and sampled

Entergy's actions for selected commitments. The bases for the review was the NRC

staff's safety evaluation report (NUREG 1905; ML080250372) issued on January 24,

2008, including Appendix A,

JAFN [[]]

PP License Renewal Commitments, and the license

renewal application (LRA) submitted on July 31, 2006.

Enclosure b. Findings and Observations No findings were identified. In-Plant Observations The inspectors observed ongoing activities and inspected the general condition of SSCs

within the scope of license renewal. The inspectors performed reviews in the reactor

and turbine buildings, and of diesel fuel oil systems, as related to commitments and aging management programs (AMPs). The inspectors determined the general conditions to be satisfactory and Entergy's activities were in accordance with facility

programs and procedures. Commitments - Review Complete Commitment 7 - Heat Exchanger Monitoring Program

Commitment 7 stipulated that Entergy "Implement the Heat Exchanger Monitoring

Program as described in LRA Section B.1.15" by October 17, 2014. The inspectors reviewed the commitment closure verification, implementation plan, and Entergy corporate and FitzPatrick site procedures for eddy current testing and heat exchanger

monitoring, and discussed program implementation with the responsible program owner.

The inspectors concluded that Commitment 7 had been completed. Commitments Needing Additional NRC Review Commitment 1 - Buried Piping and Tanks Inspection Program

Commitment 1 stipulated that Entergy "Implement the Buried Piping and Tanks Inspection Program as described in LRA Section B.1.1" by October 17, 2014.

The inspectors reviewed the commitment closure verification, implementation plan, and

Entergy corporate and FitzPatrick site procedures for buried piping and tank inspections,

and discussed program implementation with the responsible program owner. The inspectors also reviewed the records from an excavation which inspected two buried pipes, and noted that plans existed for additional excavations prior to October 17, 2014.

The inspectors concluded that the specified buried pipe inspection before the period of

extended operations (PEO) had been completed but that additional NRC review of any

additional inspections before

PEO should be performed during subsequent

NRC license renewal inspections.

Commitment 3 - Diesel Fuel Monitoring Program

Commitment 3 stipulated that Entergy "Enhance the Diesel Fuel Monitoring Program to

include periodic draining, cleaning, visual inspections, and ultrasonic measurement of the bottom surfaces of the fire pump diesel fuel oil tanks,

EDG day tanks, and

EDG fuel oil tanks to ensure the significant degradation is not occurring" and "specify acceptance

criteria for ultrasonic testing (UT) measurements of the diesel generator fuel storage tanks within the scope of this program."

Enclosure The inspectors reviewed the commitment closure verification, implementation plan,

calculation

JAF -

CALC-12-00005 for the acceptance criteria, tank drawing, and procedures and work orders related to the tank cleaning and inspection. The inspectors discussed the program enhancements with the program owner and observed the

condition of the tanks in the plant. Also, the inspectors noted that periodic draining,

cleaning, and visual inspections have been performed on the EDG fuel oil tanks, but no

inspection of the other fuel oil tanks or UT tank measurements had been performed.

The inspectors determined that the calculated acceptance criteria appeared to be non-conservative, in that a corrosion allowance was included for some tank components but

not for others. The calculation stated that "since the design margin for the head portion

of the fuel oil storage tanks and the heads of the fire pump diesel fuel oil tank are so

restrictive, no additional [corrosion] allowance can be provided for these sections of the respective tanks." The calculation stated that "minimum measured UT values must be sent to Civil Design Engineering to determine Remaining Service Life" but no provision

was made to accomplish this expectation. Entergy issued

LO -

LAR-2012-00004,

Corrective Action 181 to address this concern.

The inspectors noted that the acceptance criteria calculations for the fuel oil storage tanks did not address any loads due to the fuel oil delivery truck being on the concrete

pad above the underground tanks during fuel delivery. Entergy issued

LO -

LAR-2012-

00004, Corrective Action 185 to address this concern.

The inspectors reviewed the planned frequency for the cleaning and inspection of the fuel oil tanks. Safety evaluation report (SER) Section 3.0.3.2.8 documented that Entergy stated that the underground fuel oil storage tanks have been "cleaned and inspected on

an eight-year frequency" and that Entergy "proposed to continue to inspect these tanks

on this eight-year frequency based on post inspection results." Nonetheless, the

inspectors found that model work orders specified the cleaning and inspection to be done on a ten year frequency, and this frequency has not always been met. For example, Tank 93TK-6D had a cleaning and inspection on October 15, 2001, which was

almost 12 years after the previous inspection and had the next inspection scheduled for

October 21, 2013, which will be another 12 year period. Entergy issued

LO -

LAR-2012-

00004, Corrective Actions 182 and 183 to address these concerns.

The inspectors concluded that considerable progress on this commitment had been made but that additional

NRC review of the results of the planned inspections before the
PEO and the

UT acceptance criteria should be performed during future NRC license

renewal inspections. Commitment 12 - One-Time Inspection Program

Commitment 12 stipulates that Entergy "Implement the One-Time Inspection Program as

described in LRA Section B.1.21" within the 10 years prior to October 17, 2014. The inspectors reviewed the implementation plan and Entergy corporate procedure for one-time program inspections, and discussed program implementation with the responsible program owner. The inspectors reviewed status reports, sample plans, and

records from a sample of completed inspections.

Enclosure The inspectors noted that both

LRA Section B.1.21 and

SER Section 3.0.3.1.6 address the proposed one-time inspection of the main steam flow restrictors (cast austenitic

stainless steel (CASS)). Subsequent to issuance of the renewed license, Entergy determined that the flow restrictors were fabricated of a grade of

CA [[]]

SS material which was not susceptible to cracking and removed the inspection from the sample plan. The

inspectors noted that while there was a sound technical basis for not performing the

planned inspection, Entergy had not taken any action to revise the commitment

regarding the proposed inspection. Entergy issued

LO -

LAR-2012-00004, Corrective

Action 184, to address this concern. The inspectors concluded that the One-Time Program merited additional review

following completion of the program, including the resolution of the rescinded flow

restrictor inspection.

Commitment 15 - Selective Leaching Program

Commitment 15 stipulates that Entergy "Implement the Selective Leaching Program as

described in LRA Section B.1.25" prior to October 17, 2014.

The inspectors reviewed the implementation plan and Entergy corporate procedure for selective leaching inspections, and discussed program implementation with the

responsible program owner, including a sample plan status report.

The inspectors determined that numerous selective leaching inspections were planned

for components fabricated of carbon steel, a non-susceptible material. Also, the inspectors noted that the sample plan had determined the number of samples based on material, environment and system, which represented a more extensive population of samples than proposed in FitzPatrick's

LRA and

NRC guidance (i.e., sampling based on

material and environment only). Based on these observations, Entergy stated that the

sample plan for the selective leaching program would be re-evaluated and only inspections on susceptible materials would be used.

The inspectors concluded that the Selective Leaching Program merited additional NRC

review following completion of the program, including the re-evaluated sample plan.

Commitment Summary The inspectors concluded that Entergy actions on Commitment 7 were complete and

met regulatory expectations as reflected in the staff's safety evaluation report. The

inspectors concluded that additional NRC inspection was merited on Commitments 1, 3,

2, and 15. Further NRC inspection of license renewal commitments, including the above four commitments, is planned prior to the scheduled completion date of October 17, 2014.

.2 Follow-up on Alternative Dispute Resolution Confirmatory Order (92702)

Background

NRC Confirmatory Order (
CO )
EA -10-090 /

EA-10-248 / EA-11-106 was issued to

Entergy on January 26, 2012, to confirm commitments made to the NRC during a

mediation session held on November 9, 2011. The mediation session was conducted

Enclosure upon Entergy's request, in response to the

NRC 's offer of Alternative Dispute Resolution (

ADR), regarding apparent violations identified by the NRC at FitzPatrick. As part of the

settled agreement for the CO, Entergy agreed to take additional actions to ensure that the effectiveness of corrective actions previously taken for the issues identified are extended to the Entergy fleet and to the industry.

The objective of this inspection was to verify the actions required of Entergy, to date, as

documented in the CO have been implemented. The inspectors used guidance

contained in inspection procedure 92702 to conduct the reviews. Actions required of Entergy to be completed at a later date will be inspected and documented in forthcoming inspection reports.

.A (1) Inspection Scope
CO Section V, Paragraph
4.A (2): Entergy will review its existing fleet-wide general employee training (

GET) to ensure adequate coverage of the lessons learned from the

event that formed the basis for the CO, regarding both procedural compliance and the

requirement to maintain complete and accurate records in accordance with 10 CFR

50.9. (2) Findings and Observations No findings were identified. As discussed in NRC Inspection Report 05000333/2012003,

Section

4OA 5.2, Entergy initiated

CR-JAF-2012-00966 to address actions to be taken in

response to the

CO. As addressed in corrective action (
CA ) 3 to this
CR , Entergy conducted a review of their fleet-wide
GET training material content with respect to lessons learned from the events that formed the basis for the CO and concluded that
FCBT -

GET-PATSS, "General Employee Training Program, Entergy Fleet Specific Plant

Access Training Lesson Plan," Revision 13, did not adequately address the need for

procedural compliance and the requirement to maintain complete and accurate records in accordance with

10 CFR 50.9. Entergy developed recommended improvements to the
GET training material under
CR -

[[::JAF-2012-00966|JAF-2012-00966]], CA 4, which were projected to be

incorporated in the lesson plan during the third quarter of 2012. The inspectors reviewed the current revision of

FCBT -

GET-PATSS, Revision 17, and

determined that Entergy had incorporated the recommended improvements to address the previous gaps in the

GET training material with respect to the
CO. This closes item 4.A.
.B (1) Inspection Scope
CO Section V, Paragraph
4.B Entergy will prepare a case study about the event that formed the basis of the

CO, highlighting the role of those who had the opportunity to

detect, report, and prevent the misconduct, as well as on the actions of the individuals

who engaged in the misconduct. The Site Vice President or General Manager for Plant

Operations at each of Entergy's nine commercial nuclear power plants will present the

case study during two station-wide meetings to ensure that both day and night shift personnel will have the opportunity to attend. Entergy will complete these presentations within 180 days of the date of the CO. Entergy will make this case study available for

NRC review before conducting these station-wide meetings.

Enclosure (2) Findings and Observations

No findings were identified. As discussed in

NRC Inspection Report 05000333/2012003, Section 4

OA5.2, the inspectors observed case study presentations at FitzPatrick and Pilgrim Nuclear Power Station. During this inspection period, the inspectors reviewed

documentation, presented in

CR -

[[::JAF-2012-00966|JAF-2012-00966]] corrective actions 22 through 30,

confirming each Entergy nuclear site had conducted the case study presentations. This

closes item

4.B. .C (1) Inspection Scope
CO Section V, Paragraph
4.D (3): Within 30 days after revising its procedure
EN -QV-136, Nuclear Safety Culture Monitoring, which implements the safety culture monitoring processes in
NEI 09-07 "Fostering a Strong Nuclear Safety Culture," Entergy will provide the results of its review to

NEI for its consideration in revising NEI document 09-07 "Fostering a Strong Nuclear Safety Culture." Entergy will make the results of this review

available for NRC review.

(2) Findings and Observations No findings were identified. As addressed in

CR -

[[::JAF-2012-00966|JAF-2012-00966]], CA 40, Entergy staff

performed a review of

EN -

QV-136, "Nuclear Safety Culture Monitoring," Revision 0, and

concluded that, in all likelihood, the procedure would not have detected the safety

culture weaknesses that led to the misconduct that formed the basis for the CO. Entergy

staff determined that the procedure should have a greater focus on data analysis, discussion of safety culture issues, and developing actions to address safety culture weaknesses, with less emphasis on data sorting and review. To incorporate

recommended changes Entergy staff developed revision 1 of

EN -

QV-136 which became

effective on July 11, 2012. Additionally, by letter dated August 3, 2012 (ML12229A542)

Entergy staff informed the

NRC of that Entergy had provided the results of its review of
NEI 09-07 to
NEI for its consideration in revising
NEI 09-07. This closes item
4.D. [[.3 (Closed) Temporary Instruction 2515/187 - Inspection of Near-Term Task Force Recommendation 2.3 Flooding Walkdowns a. Inspection Scope The inspectors verified that the licensee's walkdown packages for manhole 1 and reactor building roof drains 7-9 contained the elements specified in the]]

NEI 12-07

Walkdown Guidance document.

The inspectors accompanied FitzPatrick on their walkdown of headwalls 1 and 2 and verified that the licensee performed the following: Visual inspection for indications of degradation that would prevent the functionality of the flood protection feature Critical SSC dimensions were measured Available physical margin, where applicable, was determined.

Enclosure The inspectors independently performed a walkdown of the screenwell pump house and verified that the following:

Safety-related

SSC s and those important to safety were appropriately protected from area flooding via curbing or location above expected flood water levels The licensee followed their walkdown procedure Available physical margin was determined

CRs were written for any degraded conditions The inspectors verified that noncompliances with current licensing requirements and

issues identified in accordance with the 10 CFR 50.54(f) letter, Item 2.g of Enclosure 4, were entered into the licensee's corrective action program. In addition, issues identified in response to Item 2.g that could challenge risk significant equipment and the licensee's

ability to mitigate the consequences will be subject to additional NRC evaluation. b. Findings No findings were identified. .4 (Closed) Temporary Instruction 2515/188 - Inspection of Near-Term Task Force Recommendation 2.3 Seismic Walkdowns a. Inspection Scope The inspectors accompanied the licensee on their seismic walkdowns of the following

equipment and walkbys of the associated areas. Seismic walkdown equipment list

(SWEL) numbers are in parentheses.

'A' spent fuel pool cooling pump (SWEL 2-8), reactor building 326 foot elevation, on September 20, 2012 'D'

EDG (
SWEL 1-635),
EDG building 272 foot elevation, on September 27, 2012 4160 V switchgear Bus 10500 (
SWEL 1-430, 1-433),
EDG building 272 foot elevation, on October 31, 2012 The inspectors independently performed walkdowns of control rod drive hydraulic control unit 02-19 water accumulator (

SWEL 1-43) and the 'A' core spray pump (SWEL 1-171)

in the reactor building (272 foot and 227 foot elevations, respectively) on November 20,

2012.

The following seismic features were verified during both the accompanied and independent walkdowns, as applicable:

Anchorage was free of bent, broken, missing or loose hardware Anchorage was free of corrosion that is more than mild surface oxidation Anchorage was free of visible cracks in the concrete near the anchors Anchorage configuration was consistent with plant documentation SSCs will not be damaged from impact by nearby equipment or structures Overhead equipment, distribution systems, ceiling tiles and lighting, and masonry block walls are secure and not likely to collapse onto the equipment

Enclosure Attached lines have adequate flexibility to avoid damage The area appears to be free of potentially adverse seismic interactions that could cause flooding or spray in the area The area appears to be free of potentially adverse seismic interactions that could cause a fire in the area The area appears to be free of potentially adverse seismic interactions associated with housekeeping practices, storage of portable equipment, and temporary installations (e.g., scaffolding, lead shielding) Observations made during the walkdowns that could not be determined to be acceptable

were entered into the licensee's corrective action program for evaluation. Additionally, inspectors verified that items that could allow the spent fuel pool to drain down rapidly

were added to the

SWEL and these items were walked down by the licensee. b. Findings No findings were identified. .5 Institute of Nuclear Power Operations (

INPO) Report Review a. Inspection Scope

The inspectors reviewed the final report for the

IN [[]]

PO plant assessment of the James

A. FitzPatrick Nuclear Power Plant conducted in February 2012. The inspectors reviewed this report to ensure that any issues identified were consistent with
NRC perspectives of Entergy's performance and to determine if

INPO identified any significant safety issues that required further NRC follow-up. b. Findings No findings were identified.

.6 Follow-up Inspection for Three or More Severity Level

IV Traditional Enforcement Violations in the Same Area in a 12-Month Period (

IP 92723) a. Inspection Scope The inspectors performed a follow-up inspection in accordance with inspection

procedure (IP) 92723 for three Severity Level (SL) IV Traditional Enforcement violations

in the area of potential for impacting the Regulatory Process that occurred in the second half of 2011 and first half of 2012. Consistent with guidance in IP 92723, multiple traditional enforcement violations in the same area should result in the licensee

examining the group of violations to identify any commonalities. This follow-up inspection is designed to look at the licensee's evaluation of the group of violations.

The following traditional enforcement violations were the subject of this inspection: A

SL [[]]
IV [[]]
NCV of 10

CFR Part 50.73, "Licensee Event Report [LER] System," because a violation of TS 3.5.1.G for the condition of the high pressure coolant injection and

Enclosure reactor core isolation cooling systems being simultaneously inoperable was not reported to the

NRC within 60 days of discovery. (
IR 2012-002; March 30, 2012) A
SL [[]]
IV [[]]
NCV of 10
CFR 50.74, "Notification of Change in Operator or Senior Operator Status," because Entergy did not notify the
NRC within 30 days of discovering a change in medical condition for a licensed operator. (
IR 2012-301; April 24, 2012) A
SL [[]]
IV [[]]
NCV of 10
CFR 50.71(e) because Entergy personnel did not update the
UFSAR - Emergency Bus Voltage Consistent with Current Plant Conditions. (
IR 2011-003; June 30, 2011) The objectives of the inspection were to determine whether Entergy personnel: Provided assurance that the causes of multiple
SL [[]]
IV Traditional Enforcement violations were understood Provided assurance that the extent of condition and extent of cause of multiple
SL [[]]
IV Traditional Enforcement violations were identified Provided assurance that corrective actions for the
SL [[]]

IV Traditional Enforcement violations were sufficient to address the causes The inspectors reviewed condition reports, procedures, and relevant references to the violations. The inspectors also interviewed management and staff personnel who were

familiar with the violations and participated in the evaluation or corrective actions. b. Findings and Observations The inspectors determined that Entergy staff did not conduct a collective evaluation or

implement a systematic method to evaluate the group of violations to determine common causes or ascertain whether there were commonalities amongst the group of traditional

enforcement violations. Additionally, the inspectors did not identify relevant corrective action documentation that FitzPatrick personnel considered such a review or that the station's pre-inspection assessment identified or conducted this type of review. Based on a limited independent review expanded to include relevant information from

2010 through 2012, the inspectors identified two commonalities amongst the violations. Specifically, the inspectors noted that all three violations were

NRC -identified violations (vice self-revealing and/or licensee-identified) and had aspects that potentially indicate interface weaknesses when multiple departments interact to meet required
NRC regulatory processes/reporting items (i.e.
UFSAR /

LER reporting process). In particular,

while the inspectors did not attempt to assess whether the Licensing Department

functions were a primary or contributing cause to the NCVs, the inspectors identified that Licensing Department administrative responsibilities appeared to be involved in all three violations that impacted the regulatory process. The inspectors also identified another

prior occurrence in 2011 that would be considered to impact the regulatory processes

and similarly involved licensing department administrative responsibilities. Specifically, the inspectors noted that a minor violation regarding inaccurate

2011 NRC [[]]
PI submittals for unplanned down powers was identified and documented by the
NRC in inspection report (

IR) 05000333/2012002. The NRC identified the issue in 2011 (Unresolved Item

(URI) 2011004-01) and the

NRC and Industry's frequently asked question (

FAQ)

process determined that the station's omission of three down powers was not correct or

consistent with PI reporting guidance.

Enclosure Overall, the inspectors concluded that Entergy did not meet the inspection objectives of

NRC [[]]

IP 92723. However, the inspectors did not identify a regulatory violation or

standard that was not met. The results of this inspection may be considered by the

NRC in evaluating and dispositioning future traditional enforcement violations that impact the regulatory process or have similar performance aspects. Entergy staff issued

CR-JAF-

2012-08880 to address these observations. 4OA6 Meetings, Including Exit On January 18, 2013, the inspectors presented the inspection results to Mr. Michael Colomb, Site Vice President, and other members of the FitzPatrick staff. The inspectors

verified that no proprietary information was retained by the inspectors or documented in

this report.

ATTACH [[]]
MENT [[:]]
SUPPLE [[]]
MENTAR Y
INFORM [[]]
ATION Attachment
SUPPLE [[]]
MENTAR Y
INFORM [[]]
ATION [[]]
KEY [[]]
POINTS [[]]
OF [[]]

CONTACT Entergy Personnel

M. Colomb, Site Vice President

C. Adner, Manager, Licensing

C. Brown, Manager, Quality Assurance, Entergy B. Finn, Director, Nuclear Safety Assurance T. Hunt, Manager, Corrective Action and Assessment

K. Irving, Manager, Programs and Components Engineering

D. Poulin, Manager, Operations

T. Redfearn, Manager, Security M. Reno, Manager, Maintenance E. Riley, License Renewal Project Manager

B. Sullivan, General Manager, Plant Operations

D. Wallace, Director, Engineering
E. Wolfe, Manager, Radiation Protection
LIST [[]]
OF [[]]
ITEMS [[]]
OPENED ,
CLOSED ,
DISCUS [[]]
SED ,
AND [[]]

UPDATED

Opened/Closed 05000333/2012005-01 NCV Failure to Install Reserve Station Service Transformers in Accordance with Procedure

(Section 4OA3)05000333/2012005-02

NCV Failure of 'A'

EDG Output Breaker to Close Following Loss of Offsite Power (Section 4OA3)

05000333/2515/187

TI Inspection of Near-Term Task Force Recommendation 2.3 Flooding Walkdowns (Section 4

OA5)

05000333/2515/188

TI Inspection of Near-Term Task Force Recommendation 2.3 Seismic Walkdowns (Section 4

OA5)

Attachment

LIST [[]]
OF [[]]
DOCUME [[]]
NTS [[]]
REVIEW [[]]

ED Section 1R01: Adverse Weather Protection Procedures AOP-13, "High Winds, Hurricanes and Tornadoes," Revision 19

AP -12.04, "Seasonal Weather Preparations," Revision 19
ENS -
EP -302, "Severe Weather Response," Revision
11 OP -4, "Circulating Water System," Revision 71
OP -22, "Diesel Generator Emergency Power," Revision 58
OP -51A, "Reactor Building Ventilation and Cooling System," Revision 49
OP -60, "Diesel Generator Room Ventilation," Revision 8
SAP -19, "Severe Weather," Revision 6 Section 1R04: Equipment Alignment
ODSO -4, "Shift Turnover and Log Keeping," Revision
108 OP -20, "Standby Gas Treatment System," Revision 37
OP -21, "Emergency Service Water," Revision 38 OP-22, "Diesel Generator Emergency Power," Revision 58
OP -43A, "125

VDC Power System," Revision 27 Section 1R05: Fire Protection

Procedures

EN -
TQ -125, "Fire Brigade Drills," Revision 1
PFP -
PWR 04, "Battery Room Complex/ Elev. 272', 282' Fire Area/Zone
III /
BR -1,
BR -2,
IV /BR-3,
BR -4,
XVI /BR-5, Revision 2
PFP -
PWR 11, "Cable Spreading Room/Elev. 272' Fire Area/Zone
VII /
CS -1, Revision
2 PFP -
PWR 23, "Motor Generator Set Room/Elev. 300' Fire Area/Zone
IA /
MG -1, Revision
4 PFP -
PWR 32, "Emergency Diesel Generator Spaces-south Elev. 272' Fire Area/Zone
VI /
EG -3,
EG -4,
EG -6," Revision
5 PFP -
PWR 28, "Reactor Building/Elev. 369' Fire Area/Zone
IX /
RB -1A," Revision 7 Documents
CR -
JAF -2012-08848
JAF -

RPT-04-00478, "JAF Fire Hazards Analysis," Revision 2

Section 1R11: Licensed Operator Requalification Program

OP -65, "Startup and Shutdown Procedure," Revision 114 Section 1R12: Maintenance Effectiveness Procedures
EN -DC-203, "Maintenance Rule Program," Revision
1 EN -
DC -204, "Maintenance Rule Scope and Basis," Revision
2 EN -
DC -205, "Maintenance Rule Monitoring," Revision 4
EN -

DC-206, "Maintenance Rule (a)(1) Process," Revision 2

Attachment Documents

JENG -
APL -12-002, Maintenance Rule (a)(1) Action Plan for the Analog Transmitter Trip System, Revision 0 System Health Report for 02-3 - Nuclear Boiler Instrumentation, third quarter 2012
JAF -
RPT -NMS-02278, "Maintenance Rule Basis Document System 07 Neutron Monitoring" System Health Report for Neutron Monitoring System for fourth quarter 2011 through third quarter 2012 Work Orders WO 302288
WO 319702
WO [[]]
319704 WO 319707

WO 319708 WO 319717

Condition Reports

CR -
JAF -2010-05256
CR -
JAF -2010-06720
CR -
JAF -2010-07103
CR -
JAF -2011-00605
CR -
JAF -2011-06437
CR -
JAF -2011-06509
CR -
JAF -2012-00484
CR -
JAF -2012-02212
CR -
JAF -2012-02495
CR -
JAF -2012-02567
CR -
JAF -2012-02732
CR -
JAF -2012-03740
CR -
JAF -2012-04288
CR -
JAF -2012-05443
CR -
JAF -2012-05444
CR -
JAF -2012-05661
CR -
JAF -2012-05669
CR -
JAF -2012-05725
CR -
JAF -2012-05763
CR -
JAF -2012-05869
CR -
JAF -2012-05959
CR -
JAF -2012-06285
CR -
JAF -2012-06346
CR -
JAF -2012-06366
CR -
JAF -2012-06560
CR -
JAF -2012-06578
CR -
JAF -2012-06626
CR -
JAF -2012-06680
CR -
JAF -2012-06824
CR -
JAF -2012-06981
CR -
JAF -2012-07210
CR -
JAF -2012-07419
CR -
JAF -2012-07441
CR -
JAF -2012-07453
CR -
JAF -2012-07552
CR -
JAF -2012-07575
CR -
JAF -2012-07579
CR -
JAF -2012-07583
CR -
JAF -2012-07688
CR -
JAF -2012-07936
CR -
JAF -2012-08110
CR -
JAF -2012-08131
CR -
JAF -2012-08344
CR -
JAF -2012-08347Section 1R13: Maintenance Risk Assessments and Emergent Work Control AP-10.10, "On-Line Risk Assessment," Revision 8
EN -
OP -119, "Protected Equipment Postings," Revision 5
EN -

WM-104, "On Line Risk Assessment," Revision 7

Section 1R15: Operability Determinations and Functionality Assessments Procedures

EN -
OP -104, "Operability Determination Process," Revision 6
EN -

RE-216, "Channel-Control Blade Interference Monitoring," Revision 2 RAP-7.3.39, "Channel - Control Blade Interference Monitoring," Revision 2

Documents

ECH -
NE -12-00011, "SC 11-05 Sampling Plan," Revision 0
ECH -
NE -11-00080, "FitzPatrick C20 Channel-Control Blade Interference Monitoring Plan," Revision 2 Operability Evaluation for
CR -

[[::JAF-2011-04144|JAF-2011-04144]]

Attachment Section 1R19: Post Maintenance Testing Procedures

FPP -3.53, "Transformer 71T-2 Deluge Operability Test," Revision 2

MP-002.04, "Reactor Vessel Safety/Relief Valve (SRV) Maintenance (IST), Revision 36

RAP -7.4.01, "Control Rod Scram Time Evaluation," Revision 26
ST -1B, "

MSIV Fast Closure Test (IST)," Revision 25

ST -21F, "Main Turbine Overspeed Trip Device and Mechanical Trip Valve Test," Revision 8
ST -22K, "Manual Safety Relief Valve Operation System Test (
IST ), Revision
2 ST -39H, "
RPV System Leakage Test and
CRD Class 2 Piping Inservice Test (

ISI)," Revision 30

Documents

CR -
JAF -2012-06714
CR -
JAF -2012-07218
CR -

[[::JAF-2012-07674|JAF-2012-07674]] WO 277786

Section 1R20 Refueling and Other Outage Activities

Procedures

AP -10.09, "Outage Risk Assessment," Revision 32
OP -13D, "

RHR-Shutdown Cooling," Revision 24

OP-30A, "Refueling Water Level Control," Revision 16

OP-65, "Startup and Shutdown Procedure," Revisions 113 and 114

OSP-66.001, "Management of Refueling Activities," Revision 2 Documents R20, "Schedule Risk Assessment Based on Schedule Issued 8/6/12, dated 9/15/12," Revision 1

Section 1R22: Surveillance Testing Condition Reports

CR -
JAF -2012-05469
CR -
JAF -2012-06607
CR -
JAF -2012-06718
CR -

JAF-2012-07282Section 2RS1: Radiological Hazard Assessment and Exposure Controls

Procedures

EN -
RP -101, "Access Control for Radiologically Controlled Areas," Revision 6
EN -
RP -108, "Radiation Protection Posting," Revision 11
EN -

RP-121, "Radioactive Material Control," Revision 6 Surveys Reviewed [[::JAF-1209-0599|JAF-1209-0599]], 9/27/12

[[::JAF-1209-0563|JAF-1209-0563]], 9/26/12

JAF -1209-0579, 9/26/12
JAF -1209-0539, 9/25/12

[[::JAF-1209-0470|JAF-1209-0470]], 9/24/12 [[::JAF-1209-0522|JAF-1209-0522]], 9/24/12

JAF -1209-0120, 9/13/12
JAF -1209-0353, 9/20/12

[[::JAF-1209-0347|JAF-1209-0347]], 9/20/12 [[::JAF-1209-0339|JAF-1209-0339]], 9/20/12

JAF -1209-0335, 9/20/12
JAF -1209-0334, 9/20/12

[[::JAF-1209-0326|JAF-1209-0326]], 9/20/12 [[::JAF-1209-0322|JAF-1209-0322]], 9/20/12

JAF -1209-0301, 9/19/12
JAF -1209-0298, 9/19/12

[[::JAF-1209-0309|JAF-1209-0309]], 9/19/12 [[::JAF-1209-0291|JAF-1209-0291]], 9/19/12

JAF -1209-0292, 9/19/12
JAF -1209-0278, 9/19/12

[[::JAF-1209-0284|JAF-1209-0284]], 9/19/12 [[::JAF-1209-0273|JAF-1209-0273]], 9/18/12

[[::JAF-1209-0264|JAF-1209-0264]], 9/18/12

[[::JAF-1209-0279|JAF-1209-0279]], 9/18/12

Attachment

JAF -1209-0235, 9/17/12
JAF -1209-0223, 9/17/12
JAF -1209-0216, 9/17/12
JAF -1209-0210, 9/17/12
JAF -1209-0191, 9/17/12
JAF -1209-0185, 9/17/12
JAF -1209-0183, 9/17/12
JAF -1209-0167, 9/16/12
JAF -1209-0165, 9/16/12
JAF -1209-0162, 9/16/12
JAF -1209-0161, 9/16/12 Condition Reports
CR -JAF-2012-05505
CR -
JAF -2012-05523
CR -
JAF -2012-05528
CR -
JAF -2012-05539
CR -
JAF -2012-05589
CR -
JAF -2012-05591
CR -
JAF -2012-05594
CR -
JAF -2012-05611
CR -
JAF -2012-05622
CR -
JAF -2012-05666 Section
2RS 2: Occupational
ALARA Planning and Controls Procedures
EN -
RP -110, "ALARA Program," Revision 9
EN -
RP -110-1, "ALARA Initiative Deferrals," Revision
1 EN -
RP -110-4, "Radiation Protection Risk Assessment Process," Revision
2 EN -
RP -121, "Radioactive Material Control," Revision 6 Condition Report
CR -

[[::JAF-2012-05595|JAF-2012-05595]]

Section:

2RS 3: In-Plant Airborne Radioactivity Control and Mitigation Procedures

EN-RP-131, "Air Sampling," Revision 9

Air Samples Reviewed

Sampler Number Survey Number Date 1146 120125 9/19/12 1115 120225 9/25/12

1114 120226 9/25/12

1114 120227 9/25/12

Section 4OA2: Identification and Resolution of Problems

Procedures

EN -
LI -102, "Corrective Action Process," Revision 19
EN -
LI -121, "Entergy Trending Process," Revision 12
EN -
OP -117, "Operations Assessments," Revision 4 Condition Reports
CR -
JAF -2012-03300
CR -
JAF -2012-03323
CR -
JAF -2012-03405
CR -
JAF -2012-03415
CR -
JAF -2012-03441
CR -
JAF -2012-03503
CR -
JAF -2012-03521
CR -
JAF -2012-03560
CR -
JAF -2012-03752
CR -
JAF -2012-03786
CR -
JAF -2012-03844
CR -
JAF -2012-03863
CR -
JAF -2012-04017
CR -
JAF -2012-04043
CR -
JAF -2012-04054
CR -
JAF -2012-04198
CR -
JAF -2012-04217
CR -
JAF -2012-04296
CR -
JAF -2012-04313
CR -
JAF -2012-04448
CR -

[[::JAF-2012-04455|JAF-2012-04455]]

Attachment

CR -
JAF -2012-04473
CR -
JAF -2012-04485
CR -
JAF -2012-04486
CR -
JAF -2012-04509
CR -
JAF -2012-04510
CR -
JAF -2012-04514
CR -
JAF -2012-04948
CR -
JAF -2012-05174
CR -
JAF -2012-05233
CR -
JAF -2012-05239
CR -
JAF -2012-05315
CR -
JAF -2012-05398
CR -
JAF -2012-05444
CR -
JAF -2012-05661
CR -
JAF -2012-05725
CR -
JAF -2012-05763
CR -
JAF -2012-06285
CR -
JAF -2012-06346
CR -
JAF -2012-06366
CR -
JAF -2012-06403
CR -
JAF -2012-06492
CR -
JAF -2012-06835
CR -
JAF -2012-07370
CR -
JAF -2012-07518
CR -
JAF -2012-07662
CR -
JAF -2012-07759
CR -
JAF -2012-07882
CR -
JAF -2012-07985
CR -
JAF -2012-08040
CR -
JAF -2012-08643CR-JAF-2012-08880
CR -
JAF -2012-06558
CR -
JAF -2012-06632
CR -
JAF -2012-06718
CR -
JAF -2012-06743
CR -
JAF -2012-06822
CR -
JAF -2012-06824
CR -
JAF -2012-06847
CR -
JAF -2012-06900
CR -
JAF -2012-06934
CR -
JAF -2012-07011
CR -
JAF -2012-07049
CR -
JAF -2012-07135
CR -
JAF -2012-07164
CR -
JAF -2012-07252
CR -
JAF -2012-07371
CR -
JAF -2012-07378
CR -
JAF -2012-07515
CR -
JAF -2012-07656
CR -
JAF -2012-07674
CR -
JAF -2012-07735
CR -
JAF -2012-07754
CR -
JAF -2012-07768
CR -
JAF -2012-07792
CR -
JAF -2012-07799
CR -
JAF -2012-07815
CR -
JAF -2012-08050
CR -
JAF -2012-08137
CR -
JAF -2012-08265
CR -
JAF -2012-08344
CR -
JAF -2012-08464
CR -
JAF -2012-08466 Documents
LO -
WTJAF -2012-0193
WO 00320090 Operations Performance Summaries (
PI s) for June through November 2012 Section
4OA 3: Follow-Up of Events and Notices of Enforcement Discretion
AP -03.01, "Post Transient Evaluation," Revision
13 CR -

[[::JAF-2012-7901|JAF-2012-7901]] OP-11A, "Main Generator, Transformers and Isolated Bus Phase Cooling," Revision 43

OP-65, "Startup and Shutdown Procedure," Revision 114

ST-22F, "Main Turbine Overspeed Trip Device and Mechanical Trip Valve Test," Revision 8

Section

4OA 5: Other Activities Documents
CR -JAF-2012-996
CA 39, "Snapshot Assessment/Benchmark on
EN -QV-136 Safety Culture Monitoring"
EN -
QV -136, "Nuclear Safety Culture Monitoring," Revision
1 ENOC -12-00024, "
NRC Confirmatory Order
EA -10-248,
EA -11-106 Section
V.D Review and Revision of

EN-QV-136," dated August 3, 2012

Commitment 1 (Buried Piping and Tanks) A-18341, "Commitment Closure Verification Form," April 27, 2012

JAF -
RPT -09-LR001, "Buried Piping and Tanks Inspection
AMP Implementation," Revision 0

EN-DC-343, "Underground Piping and Tank Inspection and Monitoring Program," Revision 4 B12UT016, "UT Examination of 10" CST yard piping," August 1, 2012

B12UT017, "UT Examination of 12" CST yard piping," August 1, 2012

Buried Piping General Visual Inspection - 10"CST yard piping, August 1, 2012

Attachment Buried Piping General Visual Inspection - 12"CST yard piping, August 1, 2012 LinTec, Underground Piping Inspection - 10"

CST /

HPCI, August 6, 2012

LinTec, Underground Piping Inspection - 12"

CST /
CS , August 2,
2012 LO -

LAR-2012-00004, Corrective Action 186

Commitment 3 (Diesel Fuel) A-18345, "Commitment Closure Verification Form," May 3, 2012

JAF -

RPT-09-LR009, "Diesel Fuel Monitoring AMP Implementation," Revision 0

Calculation

JAF -
CAL -12-00005, "Required Wall Thickness for Fuel Oil Storage Tanks, Fuel Oil Day Tanks, and Fire Pump Diesel Oil Tank," Revision 0 Drawing 11825-FV-17A, "Fuel Oil Storage Tanks; 93-TK-6A,-6B,-6C, and -6D," Revision 4
CEP -
NDE -0505, "Ultrasonic Thickness Examination," Revision 4
EN -

WM-105, "Clean and inspect EDG day tank"

Model

WO 000290314, Drain, clean, inspect and
UT day tank (93-TK-7A) Model
WO 51188388, Underground fuel tank (93-
TK -6A) - clean and
UT [[]]

WM-105-00, Clean and inspect fuel oil tank

Record of diesel fuel oil storage tank cleanings/VT available through electronic search, October 3,

2012 LO -
LAR -2012-00004, Corrective Actions 181, 182, 183, 185 Commitment 7 (Heat Exchangers) A-18349, "Commitment Closure Verification Form"
JAF -
RPT -09-LR015, "Heat Exchanger Monitoring Program Implementation," Revision 0
EN -
DC -316, "Heat Exchanger Performance and Condition Monitoring," Revision 3
SEP -
HX -JAF-001, "Eddy Current Testing of Heat Exchangers," Revision
0 LO -

WTJAF-2011-00124

Commitment 12 (One-Time Inspection)

JAF -
RPT -09-LR021, "One-Time Inspection AMP Implementation," Revision 0
EN -
FAP -LR-024, "One-Time Inspection," Revision
0 JAF [[]]

OTI Status Report, October 1, 2012 Completed One-Time Inspections, October 1, 2012

Remaining One-Time Inspections, October 1, 2012

OTI by Environment Sample Plan, October 4, 2012
OTI Inspection 52216405-01: C

EDG fuel oil duplex filters 4C and 5C

Commitment 15 (Selective Leaching) A-18357, "Commitment Closure Verification Form," April 7, 2012

JAF -
RPT -09-LR025, "Selective Leaching Program Implementation," Revision 0
EN -

FAP-LR-025, "Selective Leaching Inspection," Revision 3

Leaching

WO Inspections, October 4, 2012 Miscellaneous

NRC Inspection Report 05000333/2011-004

NRC Inspection Report 05000333/2011-005

NRC Inspection Report 05000333/2012-002
NRC Inspection Report 05000333/2012-003 www.nrc.gov/
NRR /Oversight/Assess/Fitz/fitz_pi for #Q/2012
EN -
LI -114,
NRC Performance Indicator Technique/Data Sheet - 3rd Quarter 2012
MSPI /WANO
PI Data Sheets for Emergency

AC - EDG (September 2011 - August 2012) and associated station narrative logs

Attachment Selected

EDG Demand Logs between September 2011 and August 2012
MSPI /WANO
PI Data Sheets for Cooling Water Support Systems -
ESW &
RHRSW (September 2011 - August 2012) and associated station narrative logs
MSPI /WANO
PI Data Sheets for High Pressure Injection -
HPCI (September 2011 - August 2012) and associated station narrative logs
MSPI /
WANO [[]]
PI Data Sheets for Residual Heat Removal -
RHR (September 2011 - August 2012) and associated station narrative logs
MSPI /
WANO [[]]
PI Data Sheets for Heat Removal -
RCIC (September 2011 - August 2012) and associated station narrative logs
LO -

HQNLO-2007-0076, Corrective Action 11

Attachment

LIST [[]]
OF [[]]
ACRONY [[]]
MS 10 CFR Title 10, Code of Federal Regulations
ADAMS Agencywide Documents Access and Management System
ADR alternative dispute resolution
ALA [[]]
RA as low as is reasonably achievable
AMP aging management program

BWR boiling water reactor CA corrective action

CAM continuous air monitor

CAP corrective action program
CASS cast austenitic stainless steel

CO confirmatory order CR condition report

CST condensate storage tank

CT current transformer
DHR decay heat removal

EC engineering change EDG emergency diesel generator

Entergy Entergy Nuclear Northeast

EPD electronic personal dosimeter

ESW emergency service water
FAQ frequently asked question FitzPatrick James A. FitzPatrick Nuclear Power Plant
GET general employee training
HP [[]]

CI high pressure coolant injection

HRA high radiation area
IMC inspection manual chapter

INPO Institute of Nuclear Power Operations IP inspection procedure

IR inspection report
ISI in-service inspection
IST in-service test
KV kilovolt
LER licensee event report
LH [[]]

RA locked high radiation area

LRA license renewal application
MS [[]]
IV main steam isolation valve
MSPI mitigating systems performance index

NCV non-cited violation NEI Nuclear Energy Institute

NRC Nuclear Regulatory Commission
NS [[]]
ST normal station service transformer
PA [[]]
RS Publicly Available Records
PEO period of extended operations

PI performance indicator PMT post-maintenance test

PWR pressurized water reactor

Attachment R20 refueling outage

20 RCIC reactor core isolation cooling
RG Regulatory Guide
RHR residual heat removal
RP radiation protection
RS [[]]

ST reserve station service transformer

RWP radiation work permit

SDP significant determination process
SER safety evaluation report

SGT standby gas treatment SL severity level

SRV safety relief valve

SSC structure, system, or component
ST surveillance test
SWEL seismic walkdown equipment list TS technical specification
UFS [[]]

AR updated final safety analysis report

URI unresolved item
UT ultrasonic testing
VAC volt alternating current
VH [[]]
RA very high radiation area
WA [[]]

NO World Association of Nuclear Operators

WO work order