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Category:INSPECTION REPORT
MONTHYEARIR 05000254/19990171999-09-15015 September 1999 Insp Repts 50-254/99-17 & 50-265/99-17 on 990823-27.No Violations Noted.Major Areas Inspected:Pilot Baseline Insp for Annual Review of Changes to Safety Analysis Rept & Biennial Review Permanent Plant Mod IR 05000254/19990151999-08-25025 August 1999 Insp Repts 50-254/99-15 & 50-265/99-15 on 990816-20.No Violations Noted.Major Areas Inspected:Maint Rule Implementation IR 05000254/19990101999-08-20020 August 1999 Insp Repts 50-254/99-10,50-265/99-10,50-454/99-09, 50-455/99-09,50-456/99-10 & 50-457/99-10 on 990628-0721. Major Areas Inspected:Licensee C/A Approach & Implementation of Configuration Control Processes at Each Site IR 05000254/19990161999-08-19019 August 1999 Insp Repts 50-254/99-16 & 50-265/99-16 on 990719-22. Violations Noted.Major Areas Inspected:Physical Protection Cornerstone,Including Review of Access Authoization Program & Changes to Security Plan IR 05000254/19990121999-08-13013 August 1999 Insp Repts 50-254/99-12 & 50-265/99-12 on 990628-0716. Violations Noted.Major Areas Inspected:Corrective Action Process Which Included Methods Used for Identification, Cause Investigation & Correction of Quality Related Items IR 05000254/19990111999-08-13013 August 1999 Insp Repts 50-254/99-11 & 50-265/99-11 on 990601-0720.NCVs Noted.Major Areas Inspected:Performance in Initiating Events,Mitigating Sys,Barrier Integrity Cornerstones & Performance Indicator Verification IR 05000254/19990141999-07-30030 July 1999 Insp Repts 50-254/99-14 & 50-265/99-14 on 990713-15.One Violation Noted & Treated as Ncv.Major Areas Inspected: Heat Sink Performance,Which Covers Inspectable Area Under Initiating Events & Mitigation Sys IR 05000254/19990131999-07-29029 July 1999 Insp Repts 50-254/99-13 & 50-265/99-13 on 990628-0702.No Violations Noted.Major Areas Inspected:Public Radiation Safety & Review of Gaseous & Liquid Radiological Effluents & of Radiological Environmental Monitoring Program IR 05000254/19990091999-06-23023 June 1999 Insp Repts 50-254/99-09 & 50-265/99-09 on 990421-0531.One Violation of NRC Requirements Occurred & Being Treated as non-cited Violation.Major Areas Inspected:Aspects of Licensee Operations,Engineering,Maint & Plant Support IR 05000254/19990061999-05-14014 May 1999 Insp Repts 50-254/99-06 & 50-265/99-06 on 990307-0420.Three Violations Noted & Being Treated as non-cited Violations. Major Areas Insptected:Aspects of Licensee Operations,Maint, Engineering & Plant Support IR 05000254/19990081999-05-11011 May 1999 Insp Repts 50-254/99-08 & 50-265/99-08 on 990419-23.No Violations Noted.Major Areas Inspected:Adequacy of Licensee Programs,Procedures,Training & Supporting Documentation IR 05000254/19990031999-04-0909 April 1999 Insp Repts 50-254/99-03 & 50-265/99-03 on 990308-12.No Violations Noted.Major Areas Inspected:Maint & Engineering IR 05000254/19990011999-04-0101 April 1999 Insp Repts 50-254/99-01 & 50-265/99-01 on 990121-0306. Violations Noted.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support IR 05000254/19990071999-03-31031 March 1999 Radiation Protection Insp Repts 50-254/99-07 & 50-265/99-07 on 990309-12.No Violations Noted.Major Areas Inspected:Solid Radwaste Processing & Control Program & Radioactive Matls Shipping Program IR 05000254/19980211999-03-0505 March 1999 Insp Repts 50-254/98-21 & 50-265/98-21 on 981112-1218. Violation Noted:Major Areas Inspected:Isi Activities at Plant During Refueling Outage 15 IR 05000254/19990041999-02-26026 February 1999 Insp Repts 50-254/99-04 & 50-265/99-04 on 990201-05.No Violations Noted.Major Areas Inspected:Emergency Prepardeness Program as Aspect of Plant Support IR 05000254/19990021999-02-25025 February 1999 Insp Repts 50-254/99-02 & 50-265/99-02 on 990125-29.No Violations Noted.Major Areas Inspected:Radiation Protection & Chemistry Program Included Water Chemistry Control, Instrument Quality Control & internal-lab Comparison IR 05000254/19980241999-01-14014 January 1999 Partially Withheld Security Insp Repts 50-254/98-24 & 50-265/98-24.Violations Noted.Major Areas Inspected:Plant Support Activities Re Physical Protection of Quad Cities Facility.Details Withheld (Ref 10CFR2.790) IR 05000254/19980201998-12-28028 December 1998 Insp Repts 50-254/98-20 & 50-265/98-20 on 981014-1201.No Violations Noted.Major Areas Inspected:Operations,Maint & Plant Support IR 05000254/19980221998-12-28028 December 1998 Insp Repts 50-254/98-22 & 50-265/98-22 on 981130-1204.No Violations Noted.Major Areas Inspected:Radiation Protection Staff Preparation for Q1R15 Refueling Outage,Including Review of ALARA Planning & Work Plan Integration IR 05000254/19980191998-12-18018 December 1998 Insp Repts 50-254/98-19 & 50-265/98-19 on 981019-1106. Violations Noted.Major Areas Inspected:Effectiveness of Engineering & Technical Support Provided to Plant in Performance of Routine & Reactive Site Activities IR 05000254/19980171998-11-0505 November 1998 Insp Repts 50-254/98-17 & 50-265/98-17 on 980902-1014.No Violations Noted.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support IR 05000254/19980181998-10-15015 October 1998 Partially Withheld Insp Repts 50-254/98-18 & 50-265/98-18 on 980914-18 (Ref 10CFR73.71).No Violations Identified.Major Areas Inspected:Review of Plant Support Activities,Security Activities Re Onsite Personnel Access & Communications IR 05000254/19980131998-09-22022 September 1998 Insp Repts 50-254/98-13 & 50-265/98-13 on 980716-0901.No Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000254/19980141998-09-17017 September 1998 Insp Repts 50-254/98-14 & 50-265/98-14 on 980825-28.No Violations Noted.Major Areas Inspected:Evaluation of Licensee Performance During Plant Biennial Exercise of Emergency Plan IR 05000254/19980161998-09-0404 September 1998 Insp Repts 50-254/98-16 & 50-265/98-16 on 980810-14.No Violations Noted.Major Areas Inspected:Radiation Protection Program Included External & Internal Exposure Control,Whole Body Counting & Contamination & Survey Monitoring Program IR 05000254/19980151998-07-31031 July 1998 Insp Repts 50-254/98-15 & 50-265/98-15 on 980721-24.No Violations Noted.Major Areas Inspected:Aspects of Licensee Corrective Actions & Engineering Involvement in Corrective Actions Process IR 05000254/19980111998-07-0202 July 1998 Insp Repts 50-254/98-11 & 50-265/98-11 on 980504-22. Violations Noted.Major Areas Inspected:Quad Cities Safe Shutdown Analysis & Supporting Procedures IR 05000254/19980081998-05-11011 May 1998 Insp Repts 50-254/98-08 & 50-265/98-08 on 980407-09 & 14-17. No Violations Noted.Major Areas Inspected:Maint,Quality Assurance & Engineering IR 05000254/19982011998-05-0606 May 1998 Insp Repts 50-254/98-201 & 50-265/98-201 on 980216-0327.No Violations Noted.Major Areas Inspected:Evaluation of Capability of Selected Sys to Perform Safety Functions Required by Design Bases IR 05000254/19980101998-05-0606 May 1998 Insp Repts 50-254/98-10 & 50-265/98-10 on 980413-17.No Violations Noted.Major Areas Inspected:Liquid & Gaseous Effluent Programs,Annual Effluent Rept,Continuous Air & Area Radiation Monitors ML20217G3401998-04-23023 April 1998 Insp Repts 50-254/98-04 & 50-265/98-04 on 980211-0331. Violations Noted.Major Areas Inspected:Operations, Engineering,Maint & Plant Support IR 05000254/19980051998-04-23023 April 1998 Insp Repts 50-254/98-05 & 50-265/98-05 on 980216-0326. Violations Noted.Major Areas Inspected:Engineering,Including Allowances for Development of Emergency & Immediate Mods IR 05000254/19980071998-04-22022 April 1998 Insp Repts 50-254/98-07 & 50-265/98-07 on 980330-0403.No Violations Noted.Major Areas Inspected:Plant Support Activities Re Physical Protection of Plant,Adequacy of Security Procedures & Event Logs ML20216C2601998-03-0606 March 1998 Insp Repts 50-254/97-28 & 50-265/97-28 on 971224-980210. Violations Noted.Major Areas Inspected:Operations,Maint & Engineering IR 05000254/19970221998-02-13013 February 1998 Insp Repts 50-254/97-22 & 50-265/97-22 on 971027-1121. Violations Noted.Major Areas Inspected:Hpci Sys Operational Performance for Operations,Maintenance & Engineering IR 05000254/19980021998-02-0505 February 1998 Insp Repts 50-254/98-02 & 50-265/98-02 on 980112-16. Violations Noted.Major Areas Inspected:Review of ALARA Planning,Radiation Work Permits & Observations of Radworker Performance IR 05000254/19970261998-01-21021 January 1998 Insp Repts 50-254/97-26 & 50-265/97-26 on 971103-1223. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000254/19970241998-01-13013 January 1998 Insp Repts 50-254/97-24 & 50-265/97-24 on 971124-1202.No Violations Noted.Major Areas Inspected:Licensed RO & SRO Requalification Training Programs ML20197F5741997-12-23023 December 1997 Insp Repts 50-254/97-27 & 50-265/97-27 on 971103-07 & 1204. Violations Noted.Major Areas Inspected:Maint & Engineering IR 05000254/19970141997-12-16016 December 1997 Insp Repts 50-254/97-14 & 50-265/97-14 on 970729-0922.NOV & Deviations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support Re Troubleshooting Resulting in Discovery of Long Standing Problem W/Fire Pump IR 05000254/19970251997-12-0909 December 1997 Insp Repts 50-254/97-25 & 50-265/97-25 on 971103-07.No Violations Noted.Major Areas Inspected:Respiratory Protection Plan,Source Term Reduction Efforts & Follow Up on Several Open Items IR 05000254/19970211997-12-0909 December 1997 Insp Repts 50-254/97-21 & 50-265/97-21 on 970923-1103.No Violations Noted.Major Areas Inspected:Operation,Maint, Engineering & Plant Support IR 05000254/19970191997-11-18018 November 1997 Insp Repts 50-254/97-19 & 50-265/97-19 on 971006-10.No Violations Noted.Major Areas Inspected:Ep Program IR 05000254/19970181997-11-10010 November 1997 Insp Repts 50-254/97-18 & 50-265/97-18 on 970922-25. Violations Noted.Major Areas Inspected:Maintenance & Engineering IR 05000254/19970161997-11-0505 November 1997 Insp Repts 50-254/97-16 & 50-265/97-16 on 970825-29. Violations Noted.Major Areas Inspected:Fire Protection Program & Several App R Issues IR 05000254/19970201997-10-25025 October 1997 Insp Repts 50-254/97-20 & 50-265/97-20 on 970929-1002.No Violations Noted.Major Areas Inspected:Quality of Security Related Audits,Reviewed Effectiveness of Mgt Controls & Verified Performance of Protected Area Control Activities IR 05000254/19970151997-09-0303 September 1997 Insp Repts 50-254/97-15 & 50-265/97-15 on 970811-14.No Violations Noted.Major Areas Inspected:Station Chemistry & REMP IR 05000254/19970121997-07-31031 July 1997 Insp Repts 50-254/97-12 & 50-265/97-12 on 970707-16.No Violations Noted.Major Areas Inspected:Review of Plant Support Activities Re Physical Protection of Facility & Corrective Actions to Security Issues IR 05000254/19970081997-07-11011 July 1997 Insp Repts 50-254/97-08 & 50-265/97-08 on 970506-0616. Violations Noted.Major Areas Inspected:Operations,Maint & Surveillance,Engineering & Plant Support 1999-09-15
[Table view] Category:NRC-GENERATED
MONTHYEARIR 05000254/19990171999-09-15015 September 1999 Insp Repts 50-254/99-17 & 50-265/99-17 on 990823-27.No Violations Noted.Major Areas Inspected:Pilot Baseline Insp for Annual Review of Changes to Safety Analysis Rept & Biennial Review Permanent Plant Mod IR 05000254/19990151999-08-25025 August 1999 Insp Repts 50-254/99-15 & 50-265/99-15 on 990816-20.No Violations Noted.Major Areas Inspected:Maint Rule Implementation IR 05000254/19990101999-08-20020 August 1999 Insp Repts 50-254/99-10,50-265/99-10,50-454/99-09, 50-455/99-09,50-456/99-10 & 50-457/99-10 on 990628-0721. Major Areas Inspected:Licensee C/A Approach & Implementation of Configuration Control Processes at Each Site IR 05000254/19990161999-08-19019 August 1999 Insp Repts 50-254/99-16 & 50-265/99-16 on 990719-22. Violations Noted.Major Areas Inspected:Physical Protection Cornerstone,Including Review of Access Authoization Program & Changes to Security Plan IR 05000254/19990121999-08-13013 August 1999 Insp Repts 50-254/99-12 & 50-265/99-12 on 990628-0716. Violations Noted.Major Areas Inspected:Corrective Action Process Which Included Methods Used for Identification, Cause Investigation & Correction of Quality Related Items IR 05000254/19990111999-08-13013 August 1999 Insp Repts 50-254/99-11 & 50-265/99-11 on 990601-0720.NCVs Noted.Major Areas Inspected:Performance in Initiating Events,Mitigating Sys,Barrier Integrity Cornerstones & Performance Indicator Verification IR 05000254/19990141999-07-30030 July 1999 Insp Repts 50-254/99-14 & 50-265/99-14 on 990713-15.One Violation Noted & Treated as Ncv.Major Areas Inspected: Heat Sink Performance,Which Covers Inspectable Area Under Initiating Events & Mitigation Sys IR 05000254/19990131999-07-29029 July 1999 Insp Repts 50-254/99-13 & 50-265/99-13 on 990628-0702.No Violations Noted.Major Areas Inspected:Public Radiation Safety & Review of Gaseous & Liquid Radiological Effluents & of Radiological Environmental Monitoring Program IR 05000254/19990091999-06-23023 June 1999 Insp Repts 50-254/99-09 & 50-265/99-09 on 990421-0531.One Violation of NRC Requirements Occurred & Being Treated as non-cited Violation.Major Areas Inspected:Aspects of Licensee Operations,Engineering,Maint & Plant Support IR 05000254/19990061999-05-14014 May 1999 Insp Repts 50-254/99-06 & 50-265/99-06 on 990307-0420.Three Violations Noted & Being Treated as non-cited Violations. Major Areas Insptected:Aspects of Licensee Operations,Maint, Engineering & Plant Support IR 05000254/19990081999-05-11011 May 1999 Insp Repts 50-254/99-08 & 50-265/99-08 on 990419-23.No Violations Noted.Major Areas Inspected:Adequacy of Licensee Programs,Procedures,Training & Supporting Documentation IR 05000254/19990031999-04-0909 April 1999 Insp Repts 50-254/99-03 & 50-265/99-03 on 990308-12.No Violations Noted.Major Areas Inspected:Maint & Engineering IR 05000254/19990011999-04-0101 April 1999 Insp Repts 50-254/99-01 & 50-265/99-01 on 990121-0306. Violations Noted.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support IR 05000254/19990071999-03-31031 March 1999 Radiation Protection Insp Repts 50-254/99-07 & 50-265/99-07 on 990309-12.No Violations Noted.Major Areas Inspected:Solid Radwaste Processing & Control Program & Radioactive Matls Shipping Program IR 05000254/19980211999-03-0505 March 1999 Insp Repts 50-254/98-21 & 50-265/98-21 on 981112-1218. Violation Noted:Major Areas Inspected:Isi Activities at Plant During Refueling Outage 15 IR 05000254/19990041999-02-26026 February 1999 Insp Repts 50-254/99-04 & 50-265/99-04 on 990201-05.No Violations Noted.Major Areas Inspected:Emergency Prepardeness Program as Aspect of Plant Support IR 05000254/19990021999-02-25025 February 1999 Insp Repts 50-254/99-02 & 50-265/99-02 on 990125-29.No Violations Noted.Major Areas Inspected:Radiation Protection & Chemistry Program Included Water Chemistry Control, Instrument Quality Control & internal-lab Comparison IR 05000254/19980241999-01-14014 January 1999 Partially Withheld Security Insp Repts 50-254/98-24 & 50-265/98-24.Violations Noted.Major Areas Inspected:Plant Support Activities Re Physical Protection of Quad Cities Facility.Details Withheld (Ref 10CFR2.790) IR 05000254/19980201998-12-28028 December 1998 Insp Repts 50-254/98-20 & 50-265/98-20 on 981014-1201.No Violations Noted.Major Areas Inspected:Operations,Maint & Plant Support IR 05000254/19980221998-12-28028 December 1998 Insp Repts 50-254/98-22 & 50-265/98-22 on 981130-1204.No Violations Noted.Major Areas Inspected:Radiation Protection Staff Preparation for Q1R15 Refueling Outage,Including Review of ALARA Planning & Work Plan Integration IR 05000254/19980191998-12-18018 December 1998 Insp Repts 50-254/98-19 & 50-265/98-19 on 981019-1106. Violations Noted.Major Areas Inspected:Effectiveness of Engineering & Technical Support Provided to Plant in Performance of Routine & Reactive Site Activities IR 05000254/19980171998-11-0505 November 1998 Insp Repts 50-254/98-17 & 50-265/98-17 on 980902-1014.No Violations Noted.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support IR 05000254/19980181998-10-15015 October 1998 Partially Withheld Insp Repts 50-254/98-18 & 50-265/98-18 on 980914-18 (Ref 10CFR73.71).No Violations Identified.Major Areas Inspected:Review of Plant Support Activities,Security Activities Re Onsite Personnel Access & Communications IR 05000254/19980131998-09-22022 September 1998 Insp Repts 50-254/98-13 & 50-265/98-13 on 980716-0901.No Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000254/19980141998-09-17017 September 1998 Insp Repts 50-254/98-14 & 50-265/98-14 on 980825-28.No Violations Noted.Major Areas Inspected:Evaluation of Licensee Performance During Plant Biennial Exercise of Emergency Plan IR 05000254/19980161998-09-0404 September 1998 Insp Repts 50-254/98-16 & 50-265/98-16 on 980810-14.No Violations Noted.Major Areas Inspected:Radiation Protection Program Included External & Internal Exposure Control,Whole Body Counting & Contamination & Survey Monitoring Program IR 05000254/19980151998-07-31031 July 1998 Insp Repts 50-254/98-15 & 50-265/98-15 on 980721-24.No Violations Noted.Major Areas Inspected:Aspects of Licensee Corrective Actions & Engineering Involvement in Corrective Actions Process IR 05000254/19980111998-07-0202 July 1998 Insp Repts 50-254/98-11 & 50-265/98-11 on 980504-22. Violations Noted.Major Areas Inspected:Quad Cities Safe Shutdown Analysis & Supporting Procedures IR 05000254/19980081998-05-11011 May 1998 Insp Repts 50-254/98-08 & 50-265/98-08 on 980407-09 & 14-17. No Violations Noted.Major Areas Inspected:Maint,Quality Assurance & Engineering IR 05000254/19982011998-05-0606 May 1998 Insp Repts 50-254/98-201 & 50-265/98-201 on 980216-0327.No Violations Noted.Major Areas Inspected:Evaluation of Capability of Selected Sys to Perform Safety Functions Required by Design Bases IR 05000254/19980101998-05-0606 May 1998 Insp Repts 50-254/98-10 & 50-265/98-10 on 980413-17.No Violations Noted.Major Areas Inspected:Liquid & Gaseous Effluent Programs,Annual Effluent Rept,Continuous Air & Area Radiation Monitors ML20217G3401998-04-23023 April 1998 Insp Repts 50-254/98-04 & 50-265/98-04 on 980211-0331. Violations Noted.Major Areas Inspected:Operations, Engineering,Maint & Plant Support IR 05000254/19980051998-04-23023 April 1998 Insp Repts 50-254/98-05 & 50-265/98-05 on 980216-0326. Violations Noted.Major Areas Inspected:Engineering,Including Allowances for Development of Emergency & Immediate Mods IR 05000254/19980071998-04-22022 April 1998 Insp Repts 50-254/98-07 & 50-265/98-07 on 980330-0403.No Violations Noted.Major Areas Inspected:Plant Support Activities Re Physical Protection of Plant,Adequacy of Security Procedures & Event Logs ML20216C2601998-03-0606 March 1998 Insp Repts 50-254/97-28 & 50-265/97-28 on 971224-980210. Violations Noted.Major Areas Inspected:Operations,Maint & Engineering IR 05000254/19970221998-02-13013 February 1998 Insp Repts 50-254/97-22 & 50-265/97-22 on 971027-1121. Violations Noted.Major Areas Inspected:Hpci Sys Operational Performance for Operations,Maintenance & Engineering IR 05000254/19980021998-02-0505 February 1998 Insp Repts 50-254/98-02 & 50-265/98-02 on 980112-16. Violations Noted.Major Areas Inspected:Review of ALARA Planning,Radiation Work Permits & Observations of Radworker Performance IR 05000254/19970261998-01-21021 January 1998 Insp Repts 50-254/97-26 & 50-265/97-26 on 971103-1223. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000254/19970241998-01-13013 January 1998 Insp Repts 50-254/97-24 & 50-265/97-24 on 971124-1202.No Violations Noted.Major Areas Inspected:Licensed RO & SRO Requalification Training Programs ML20197F5741997-12-23023 December 1997 Insp Repts 50-254/97-27 & 50-265/97-27 on 971103-07 & 1204. Violations Noted.Major Areas Inspected:Maint & Engineering IR 05000254/19970141997-12-16016 December 1997 Insp Repts 50-254/97-14 & 50-265/97-14 on 970729-0922.NOV & Deviations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support Re Troubleshooting Resulting in Discovery of Long Standing Problem W/Fire Pump IR 05000254/19970251997-12-0909 December 1997 Insp Repts 50-254/97-25 & 50-265/97-25 on 971103-07.No Violations Noted.Major Areas Inspected:Respiratory Protection Plan,Source Term Reduction Efforts & Follow Up on Several Open Items IR 05000254/19970211997-12-0909 December 1997 Insp Repts 50-254/97-21 & 50-265/97-21 on 970923-1103.No Violations Noted.Major Areas Inspected:Operation,Maint, Engineering & Plant Support IR 05000254/19970191997-11-18018 November 1997 Insp Repts 50-254/97-19 & 50-265/97-19 on 971006-10.No Violations Noted.Major Areas Inspected:Ep Program IR 05000254/19970181997-11-10010 November 1997 Insp Repts 50-254/97-18 & 50-265/97-18 on 970922-25. Violations Noted.Major Areas Inspected:Maintenance & Engineering IR 05000254/19970161997-11-0505 November 1997 Insp Repts 50-254/97-16 & 50-265/97-16 on 970825-29. Violations Noted.Major Areas Inspected:Fire Protection Program & Several App R Issues IR 05000254/19970201997-10-25025 October 1997 Insp Repts 50-254/97-20 & 50-265/97-20 on 970929-1002.No Violations Noted.Major Areas Inspected:Quality of Security Related Audits,Reviewed Effectiveness of Mgt Controls & Verified Performance of Protected Area Control Activities IR 05000254/19970151997-09-0303 September 1997 Insp Repts 50-254/97-15 & 50-265/97-15 on 970811-14.No Violations Noted.Major Areas Inspected:Station Chemistry & REMP IR 05000254/19970121997-07-31031 July 1997 Insp Repts 50-254/97-12 & 50-265/97-12 on 970707-16.No Violations Noted.Major Areas Inspected:Review of Plant Support Activities Re Physical Protection of Facility & Corrective Actions to Security Issues IR 05000254/19970081997-07-11011 July 1997 Insp Repts 50-254/97-08 & 50-265/97-08 on 970506-0616. Violations Noted.Major Areas Inspected:Operations,Maint & Surveillance,Engineering & Plant Support 1999-09-15
[Table view] Category:INSPECTION REPORT
MONTHYEARIR 05000254/19990171999-09-15015 September 1999 Insp Repts 50-254/99-17 & 50-265/99-17 on 990823-27.No Violations Noted.Major Areas Inspected:Pilot Baseline Insp for Annual Review of Changes to Safety Analysis Rept & Biennial Review Permanent Plant Mod IR 05000254/19990151999-08-25025 August 1999 Insp Repts 50-254/99-15 & 50-265/99-15 on 990816-20.No Violations Noted.Major Areas Inspected:Maint Rule Implementation IR 05000254/19990101999-08-20020 August 1999 Insp Repts 50-254/99-10,50-265/99-10,50-454/99-09, 50-455/99-09,50-456/99-10 & 50-457/99-10 on 990628-0721. Major Areas Inspected:Licensee C/A Approach & Implementation of Configuration Control Processes at Each Site IR 05000254/19990161999-08-19019 August 1999 Insp Repts 50-254/99-16 & 50-265/99-16 on 990719-22. Violations Noted.Major Areas Inspected:Physical Protection Cornerstone,Including Review of Access Authoization Program & Changes to Security Plan IR 05000254/19990121999-08-13013 August 1999 Insp Repts 50-254/99-12 & 50-265/99-12 on 990628-0716. Violations Noted.Major Areas Inspected:Corrective Action Process Which Included Methods Used for Identification, Cause Investigation & Correction of Quality Related Items IR 05000254/19990111999-08-13013 August 1999 Insp Repts 50-254/99-11 & 50-265/99-11 on 990601-0720.NCVs Noted.Major Areas Inspected:Performance in Initiating Events,Mitigating Sys,Barrier Integrity Cornerstones & Performance Indicator Verification IR 05000254/19990141999-07-30030 July 1999 Insp Repts 50-254/99-14 & 50-265/99-14 on 990713-15.One Violation Noted & Treated as Ncv.Major Areas Inspected: Heat Sink Performance,Which Covers Inspectable Area Under Initiating Events & Mitigation Sys IR 05000254/19990131999-07-29029 July 1999 Insp Repts 50-254/99-13 & 50-265/99-13 on 990628-0702.No Violations Noted.Major Areas Inspected:Public Radiation Safety & Review of Gaseous & Liquid Radiological Effluents & of Radiological Environmental Monitoring Program IR 05000254/19990091999-06-23023 June 1999 Insp Repts 50-254/99-09 & 50-265/99-09 on 990421-0531.One Violation of NRC Requirements Occurred & Being Treated as non-cited Violation.Major Areas Inspected:Aspects of Licensee Operations,Engineering,Maint & Plant Support IR 05000254/19990061999-05-14014 May 1999 Insp Repts 50-254/99-06 & 50-265/99-06 on 990307-0420.Three Violations Noted & Being Treated as non-cited Violations. Major Areas Insptected:Aspects of Licensee Operations,Maint, Engineering & Plant Support IR 05000254/19990081999-05-11011 May 1999 Insp Repts 50-254/99-08 & 50-265/99-08 on 990419-23.No Violations Noted.Major Areas Inspected:Adequacy of Licensee Programs,Procedures,Training & Supporting Documentation IR 05000254/19990031999-04-0909 April 1999 Insp Repts 50-254/99-03 & 50-265/99-03 on 990308-12.No Violations Noted.Major Areas Inspected:Maint & Engineering IR 05000254/19990011999-04-0101 April 1999 Insp Repts 50-254/99-01 & 50-265/99-01 on 990121-0306. Violations Noted.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support IR 05000254/19990071999-03-31031 March 1999 Radiation Protection Insp Repts 50-254/99-07 & 50-265/99-07 on 990309-12.No Violations Noted.Major Areas Inspected:Solid Radwaste Processing & Control Program & Radioactive Matls Shipping Program IR 05000254/19980211999-03-0505 March 1999 Insp Repts 50-254/98-21 & 50-265/98-21 on 981112-1218. Violation Noted:Major Areas Inspected:Isi Activities at Plant During Refueling Outage 15 IR 05000254/19990041999-02-26026 February 1999 Insp Repts 50-254/99-04 & 50-265/99-04 on 990201-05.No Violations Noted.Major Areas Inspected:Emergency Prepardeness Program as Aspect of Plant Support IR 05000254/19990021999-02-25025 February 1999 Insp Repts 50-254/99-02 & 50-265/99-02 on 990125-29.No Violations Noted.Major Areas Inspected:Radiation Protection & Chemistry Program Included Water Chemistry Control, Instrument Quality Control & internal-lab Comparison IR 05000254/19980241999-01-14014 January 1999 Partially Withheld Security Insp Repts 50-254/98-24 & 50-265/98-24.Violations Noted.Major Areas Inspected:Plant Support Activities Re Physical Protection of Quad Cities Facility.Details Withheld (Ref 10CFR2.790) IR 05000254/19980201998-12-28028 December 1998 Insp Repts 50-254/98-20 & 50-265/98-20 on 981014-1201.No Violations Noted.Major Areas Inspected:Operations,Maint & Plant Support IR 05000254/19980221998-12-28028 December 1998 Insp Repts 50-254/98-22 & 50-265/98-22 on 981130-1204.No Violations Noted.Major Areas Inspected:Radiation Protection Staff Preparation for Q1R15 Refueling Outage,Including Review of ALARA Planning & Work Plan Integration IR 05000254/19980191998-12-18018 December 1998 Insp Repts 50-254/98-19 & 50-265/98-19 on 981019-1106. Violations Noted.Major Areas Inspected:Effectiveness of Engineering & Technical Support Provided to Plant in Performance of Routine & Reactive Site Activities IR 05000254/19980171998-11-0505 November 1998 Insp Repts 50-254/98-17 & 50-265/98-17 on 980902-1014.No Violations Noted.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support IR 05000254/19980181998-10-15015 October 1998 Partially Withheld Insp Repts 50-254/98-18 & 50-265/98-18 on 980914-18 (Ref 10CFR73.71).No Violations Identified.Major Areas Inspected:Review of Plant Support Activities,Security Activities Re Onsite Personnel Access & Communications IR 05000254/19980131998-09-22022 September 1998 Insp Repts 50-254/98-13 & 50-265/98-13 on 980716-0901.No Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000254/19980141998-09-17017 September 1998 Insp Repts 50-254/98-14 & 50-265/98-14 on 980825-28.No Violations Noted.Major Areas Inspected:Evaluation of Licensee Performance During Plant Biennial Exercise of Emergency Plan IR 05000254/19980161998-09-0404 September 1998 Insp Repts 50-254/98-16 & 50-265/98-16 on 980810-14.No Violations Noted.Major Areas Inspected:Radiation Protection Program Included External & Internal Exposure Control,Whole Body Counting & Contamination & Survey Monitoring Program IR 05000254/19980151998-07-31031 July 1998 Insp Repts 50-254/98-15 & 50-265/98-15 on 980721-24.No Violations Noted.Major Areas Inspected:Aspects of Licensee Corrective Actions & Engineering Involvement in Corrective Actions Process IR 05000254/19980111998-07-0202 July 1998 Insp Repts 50-254/98-11 & 50-265/98-11 on 980504-22. Violations Noted.Major Areas Inspected:Quad Cities Safe Shutdown Analysis & Supporting Procedures IR 05000254/19980081998-05-11011 May 1998 Insp Repts 50-254/98-08 & 50-265/98-08 on 980407-09 & 14-17. No Violations Noted.Major Areas Inspected:Maint,Quality Assurance & Engineering IR 05000254/19982011998-05-0606 May 1998 Insp Repts 50-254/98-201 & 50-265/98-201 on 980216-0327.No Violations Noted.Major Areas Inspected:Evaluation of Capability of Selected Sys to Perform Safety Functions Required by Design Bases IR 05000254/19980101998-05-0606 May 1998 Insp Repts 50-254/98-10 & 50-265/98-10 on 980413-17.No Violations Noted.Major Areas Inspected:Liquid & Gaseous Effluent Programs,Annual Effluent Rept,Continuous Air & Area Radiation Monitors ML20217G3401998-04-23023 April 1998 Insp Repts 50-254/98-04 & 50-265/98-04 on 980211-0331. Violations Noted.Major Areas Inspected:Operations, Engineering,Maint & Plant Support IR 05000254/19980051998-04-23023 April 1998 Insp Repts 50-254/98-05 & 50-265/98-05 on 980216-0326. Violations Noted.Major Areas Inspected:Engineering,Including Allowances for Development of Emergency & Immediate Mods IR 05000254/19980071998-04-22022 April 1998 Insp Repts 50-254/98-07 & 50-265/98-07 on 980330-0403.No Violations Noted.Major Areas Inspected:Plant Support Activities Re Physical Protection of Plant,Adequacy of Security Procedures & Event Logs ML20216C2601998-03-0606 March 1998 Insp Repts 50-254/97-28 & 50-265/97-28 on 971224-980210. Violations Noted.Major Areas Inspected:Operations,Maint & Engineering IR 05000254/19970221998-02-13013 February 1998 Insp Repts 50-254/97-22 & 50-265/97-22 on 971027-1121. Violations Noted.Major Areas Inspected:Hpci Sys Operational Performance for Operations,Maintenance & Engineering IR 05000254/19980021998-02-0505 February 1998 Insp Repts 50-254/98-02 & 50-265/98-02 on 980112-16. Violations Noted.Major Areas Inspected:Review of ALARA Planning,Radiation Work Permits & Observations of Radworker Performance IR 05000254/19970261998-01-21021 January 1998 Insp Repts 50-254/97-26 & 50-265/97-26 on 971103-1223. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000254/19970241998-01-13013 January 1998 Insp Repts 50-254/97-24 & 50-265/97-24 on 971124-1202.No Violations Noted.Major Areas Inspected:Licensed RO & SRO Requalification Training Programs ML20197F5741997-12-23023 December 1997 Insp Repts 50-254/97-27 & 50-265/97-27 on 971103-07 & 1204. Violations Noted.Major Areas Inspected:Maint & Engineering IR 05000254/19970141997-12-16016 December 1997 Insp Repts 50-254/97-14 & 50-265/97-14 on 970729-0922.NOV & Deviations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support Re Troubleshooting Resulting in Discovery of Long Standing Problem W/Fire Pump IR 05000254/19970251997-12-0909 December 1997 Insp Repts 50-254/97-25 & 50-265/97-25 on 971103-07.No Violations Noted.Major Areas Inspected:Respiratory Protection Plan,Source Term Reduction Efforts & Follow Up on Several Open Items IR 05000254/19970211997-12-0909 December 1997 Insp Repts 50-254/97-21 & 50-265/97-21 on 970923-1103.No Violations Noted.Major Areas Inspected:Operation,Maint, Engineering & Plant Support IR 05000254/19970191997-11-18018 November 1997 Insp Repts 50-254/97-19 & 50-265/97-19 on 971006-10.No Violations Noted.Major Areas Inspected:Ep Program IR 05000254/19970181997-11-10010 November 1997 Insp Repts 50-254/97-18 & 50-265/97-18 on 970922-25. Violations Noted.Major Areas Inspected:Maintenance & Engineering IR 05000254/19970161997-11-0505 November 1997 Insp Repts 50-254/97-16 & 50-265/97-16 on 970825-29. Violations Noted.Major Areas Inspected:Fire Protection Program & Several App R Issues IR 05000254/19970201997-10-25025 October 1997 Insp Repts 50-254/97-20 & 50-265/97-20 on 970929-1002.No Violations Noted.Major Areas Inspected:Quality of Security Related Audits,Reviewed Effectiveness of Mgt Controls & Verified Performance of Protected Area Control Activities IR 05000254/19970151997-09-0303 September 1997 Insp Repts 50-254/97-15 & 50-265/97-15 on 970811-14.No Violations Noted.Major Areas Inspected:Station Chemistry & REMP IR 05000254/19970121997-07-31031 July 1997 Insp Repts 50-254/97-12 & 50-265/97-12 on 970707-16.No Violations Noted.Major Areas Inspected:Review of Plant Support Activities Re Physical Protection of Facility & Corrective Actions to Security Issues IR 05000254/19970081997-07-11011 July 1997 Insp Repts 50-254/97-08 & 50-265/97-08 on 970506-0616. Violations Noted.Major Areas Inspected:Operations,Maint & Surveillance,Engineering & Plant Support 1999-09-15
[Table view] Category:UTILITY
MONTHYEARIR 05000254/19900141990-10-0404 October 1990 Insp Repts 50-254/90-14 & 50-265/90-14 on 900805-0915. Violations Noted.Major Areas Inspected:Ler Review,Regional Request,Followup on TMI Action Items,Operational Safety Verification,Esf Sys & Monthly Maint Observations IR 05000254/19900121990-08-22022 August 1990 Safety Insp Repts 50-254/90-12 & 50-265/90-12 on 900617- 0804.No Violations Noted.Two Unresolved Items Noted.Major Areas Inspected:Licensee Action on Previously Identified Items,Ler Review,Regional Requests & Testing of Mods IR 05000254/19900101990-08-14014 August 1990 Insp Repts 50-254/90-10 & 50-265/90-10 on 900605-0802. Violations Noted.Major Areas Inspected:Allegation That 1/2 Emergency Diesel Generator Cooling Pump Could Not Fulfill Cooling of Diesel & ECCS Room Coolers IR 05000254/19900111990-07-13013 July 1990 Insp Repts 50-254/90-11 & 50-265/90-11 on 900611-14.No Violations or Deviations Noted.Major Areas Inspected: Licensee Radwaste Mgt Program,Including Solid,Liquid & Gaseous Wastes & Audits & Assessments IR 05000254/19900081990-07-11011 July 1990 Insp Repts 50-254/90-08 & 50-265/90-08 on 900429-0616.No Violations Noted.Major Areas Inspected:Licensee Action on Previously Identified Items,Ler Review,Operational Safety Verification & Monthly Maint Observation IR 05000254/19890241990-06-15015 June 1990 Insp Repts 50-254/89-24 & 50-265/89-24 on 891030-900518. Violations Noted.Major Areas Inspected:Local Leak Rate Test Program,Containment Integrated Leak Rate Test Procedure & Review of Licensee Actions on Previous Insp Findings IR 05000254/19900061990-05-15015 May 1990 Insp Repts 50-254/90-06 & 50-265/90-06 on 900318-0428. Violations Noted.Major Areas Inspected:Plant Operations,Esf Sys,Radiological Controls,Maint & Surveillance,Emergency Preparedness,Security & Engineering/Technical Support IR 05000237/19900141990-04-20020 April 1990 Insp Repts 50-456/90-11,50-457/90-14,50-454/90-13, 50-455/90-12,50-237/90-14,50-249/90-13,50-373/90-07, 50-374/90-08,50-254/90-07,50-265/90-07,50-295/90-10 & 50-304/90-11 on 900220-0404.No Violations Noted IR 05000254/19900051990-04-10010 April 1990 Insp Repts 50-254/90-05 & 50-265/90-04 on 900326-30.No Violations Noted.Weaknesses Re Testing of New Whole Body Counter Noted.Major Areas Inspected:Operational Radiation Protection Program,Including External Exposure Controls IR 05000254/19900021990-04-0404 April 1990 Safety Insp Repts 50-254/90-02 & 50-265/90-02 on 900128- 0317.Violation Noted.Major Areas Inspected:Licensee Actions on Previous Items,Plant Operations,Radiological Controls, Maint/Surveillance,Emergency Preparedness & Security IR 05000265/19900051990-03-30030 March 1990 Safety Insp Rept 50-265/90-05 on 900220-0322.No Violations or Deviations Noted.Major Areas Inspected:Inservice Insp Activities,Including Review of Program,Procedures,Work Activities & Insp Data IR 05000254/19900041990-03-23023 March 1990 Insp Repts 50-254/90-04 & 50-265/90-03 on 900312-16.No Violation Noted.Major Areas Inspected:Mgt Support,Security Program Plans & Audits,Protected & Vital Area Physical Barriers & Detection & Assessment Aids IR 05000254/19890281990-02-13013 February 1990 Safety Insp Repts 50-254/89-28 & 50-265/89-28 on 891217-900127.No Violations Noted.Major Areas Inspected: Licensee Actions on Previous Items,Plant Operations, Radiological Controls,Maint Surveillance & Security IR 05000254/19890251990-01-0909 January 1990 Insp Repts 50-254/89-25 & 50-265/89-25 on 891030-1214. Violations Noted.Major Areas Inspected:Mods & Design Changes Implemented During Unit 1 Outage & Recent Request from Temporary Waiver of Compliance from Tech Specs IR 05000254/19890271990-01-0505 January 1990 Insp Rept 50-254/89-27 on 891215.No Violations Noted.Major Areas Inspected:Review of Adequacy of Licensee Analysis of Reactor Feedwater Transient on Min Critical Power Ratio Safety Limit & Determination of Cause of Turbine Trip IR 05000254/19890261990-01-0505 January 1990 Safety Insp Repts 50-254/89-26 & 50-265/89-26 on 891105- 1216.Violations Noted.Major Areas Inspected:Plant Operations,Radiological Controls,Allegations,Emergency Preparedness,Security & Engineering/Technical Support IR 05000254/19890221989-11-30030 November 1989 Insp Repts 50-254/89-22 & 50-265/89-22 on 890924-1104. Violations Noted.Major Areas Inspected:Plant Operations, Radiological Controls,Maint/Surveillance,Emergency Preparedness,Security & Engineering/Technical Support IR 05000254/19890161989-08-28028 August 1989 Insp Repts 50-254/89-16 & 50-265/89-16 on 890625-0819. Violations Noted.Major Areas Inspected:Plant Operations, Radiological Controls,Maint/Surveillance,Safety Assessment/ Quality Verification,Emergency Preparedness & Security IR 05000254/19890181989-08-24024 August 1989 Physical Security Insp Repts 50-254/89-18 & 50-265/89-18 on 890814-18.No Violations Noted.Major Areas Inspected:Mgt Support,Security Program Plans,Audits,Protected & Vital Area Physical Barriers & Detection & Assessment Aids IR 05000254/19890121989-07-17017 July 1989 Insp Repts 50-254/89-12 & 50-265/89-12 on 890514-0624.One licensee-identified Violation & Two Unresolved Items Noted. Major Areas Inspected:Licensee Actions on Previous Items, Plant Operations,Emergency Preparedness & Security ML20246C3471989-06-29029 June 1989 Safety Insp Repts 50-254/89-13 & 50-265/89-13 on 890522-0608.No Violations,Deviations or Open Items Noted. Major Areas Inspected:Maint & Inservice Testing of Pumps & Valves,Including Actions in Response to NRC Bulletin 85-003 IR 05000254/19890151989-06-28028 June 1989 Insp Repts 50-254/89-15 & 50-265/89-15 on 890619-21.No Violations Noted.Major Areas Inspected:Radwaste Mgt Program, Including Solid,Liquid & Gaseous Radwastes,Audits & Assessments & Unplanned Liquid Radwaste Release IR 05000254/19890141989-06-27027 June 1989 Insp Repts 50-254/89-14 & 50-265/89-14 on 890605-09.No Violations or Deviations Noted.Major Areas Inspected: Implementation of NRC Bulletin 88-010 Requirements Re molded-case Circuit Breakers IR 05000254/19890101989-05-22022 May 1989 Insp Repts 50-254/89-10 & 50-265/89-10 on 890402-0513.No Violations Noted.Major Areas Inspected:Plant Operations, Radiological Controls,Maint/Surveillance,Emergency Preparedness,Security & Engineering/Technical Support IR 05000254/19890041989-04-13013 April 1989 Insp Repts 50-254/89-04 & 50-265/89-04 on 890205-0401.No Violations Noted.Major Areas Inspected:Plant Operations, Radiological Controls,Maint/Surveillance,Emergency Preparedness & Security IR 05000254/19890061989-03-0707 March 1989 Insp Repts 50-254/89-06 & 50-265/89-06 on 890214-17.No Violations Noted.One Potential Contamination Control Weakness Noted.Major Areas Inspected:Radiation Protection Program,Including Organization & Mgt Controls & ALARA IR 05000254/19890051989-02-27027 February 1989 Insp Repts 50-254/89-05 & 50-265/89-05 on 890206-10.No Violations Noted.Major Areas Inspected:Chemistry Program, Including Procedures,Organization & Training & Radiological Environ Monitoring Program & Qc/Qa Program in Lab IR 05000254/19880201988-10-13013 October 1988 Insp Repts 50-254/88-20 & 50-265/88-20 on 880807-0930.No Violations or Deviations Noted.Major Areas Inspected: Operations,Maint,Surveillance,Ler Review,Routine Repts, Temporary Instructions,Radiation Control & Info Notices IR 05000254/19880211988-10-0505 October 1988 Insp Repts 50-254/88-21 & 50-265/88-21 on 880222-0901. Violations Noted.Major Areas Inspected:Compliance W/App R to 10CFR50 & Review of Fire Protection Program Requirements IR 05000254/19880191988-09-22022 September 1988 Insp Repts 50-254/88-19 & 50-265/88-19 on 880830-0902.No Violations Noted.Weakness & Four Open Items Identified.Major Areas Inspected:Annual Exercise IR 05000254/19880251988-09-20020 September 1988 Insp Repts 50-254/88-25 & 50-265/88-26 on 880908-14.No Violations Noted.Major Areas Inspected:Licensee Written Practice for Nondestructive Exam Pertaining to 25% Rule Described in SNT-TC-1A ML20154L7701988-09-14014 September 1988 Corrected Pages 13 & 14 to Insp Repts 50-254/88-15 & 50-265/88-15 ML20154L9461988-09-14014 September 1988 Insp Rept 50-265/88-24 on 880826.No Violations Noted. Major Areas Inspected:Weakness Identified in Verification of Component Operability as Documented in Insp Repts 50-254/88-15 & 50-265/88-15 IR 05000254/19882001988-09-0707 September 1988 Emergency Operating Procedures Insp Rept 50-254/88-200 on 880613-30.Inadequacies & Deficiencies Noted.Major Areas Inspected:Determination If Procedures Technically Correct & Whether Procedures Could Be Carried Out & Performed IR 05000254/19880181988-07-29029 July 1988 Partially Withheld Physical Security Insp Repts 50-254/88-18 & 50-265/88-18 on 880718-21 (Ref 10CFR73.21).Noncompliances Noted.Major Areas Inspected:Security Plan & Implementing Procedures & Mgt Effectiveness IR 05000254/19880171988-07-14014 July 1988 Insp Repts 50-254/88-17 & 50-265/88-17 on 880706-07.No Violations Noted.Major Areas Inspected:Emergency Preparedness Program Areas,Including Actions on Previously Identified Items & Initiatives to Improve Program IR 05000254/19880161988-07-0101 July 1988 Insp Repts 50-254/88-16 & 50-265/88-16 on 880607-15. Violations Noted.Major Areas Inspected:Containment Integrated Leak Rate Test Procedure,Performance & Results, Local Leak Rate Test Results & LER Followup IR 05000254/19880121988-06-28028 June 1988 Insp Repts 50-254/88-12 & 50-265/88-06 on 880310-0411-12,18, 21,26-29 & 05-10,17-18 & 0601 & 20.No Violations Noted.Major Areas Inspected:Inservice Insp Activities,Including Review of Programs 73051,Procedures 73052 & Observation of Work IR 05000254/19880111988-06-21021 June 1988 Insp Repts 50-254/88-11 & 50-265/88-12 on 880422-0601. Violations Noted.Major Areas Inspected:Maint Activities & Followup on Previous Identified Insp Items Using Selected Portions of Listed Insp Modules ML20195H1591988-06-21021 June 1988 Insp Repts 50-254/88-11 & 50-265/88-12 on 880422-0601. Violations Noted.Major Areas Inspected:Maint Activities & Followup on Previous Identified Insp Items Using Selected Portions of Listed Insp Modules IR 05000254/19880131988-06-15015 June 1988 Insp Repts 50-254/88-13 & 50-265/88-13 on 880510-20. Violation Noted.Major Areas Inspected:Radwaste Mgt & Radiation Protection Programs During Refueling & Maint Outage Including Organization & Mgt Controls IR 05000254/19880091988-06-0707 June 1988 Insp Repts 50-254/88-09 & 50-265/88-10 on 880403-0604.No Violations Noted.Major Areas Inspected:Operations,Maint, Surveillance,Ler Review,Routine Repts,Temporary Instructions & Administrative Controls Affecting Quality IR 05000254/19880101988-06-0606 June 1988 Insp Repts 50-254/88-10 & 50-265/88-11 on 880418-29.No Violations Noted.Major Areas inspected:safety-related Piping Weldments,Components & Supports Selected from Plant Mod Packages & Inservice Insp Plan IR 05000254/19880071988-05-0404 May 1988 Errata to Insp Repts 50-254/88-07 & 50-265/88-08 ML20151Z6211988-04-28028 April 1988 Insp Repts 50-254/88-07 & 50-265/88-08 on 880328-0407.No Violations Noted.Major Areas Inspected:Hpci/Rcic History & Mgt Activities,Root Cause Determination & Corrective Action & Maint Activities Re HPCI & RCIC IR 05000254/19880881988-04-27027 April 1988 Insp Repts 50-254/88-88 & 50-265/88-09 on 880404-08.No Violations Noted.Major Areas Inspected:Qa & Confirmatory Measurements for in-plant Radiochemical Analyses & Verification of TLD Collocation IR 05000254/19880041988-04-12012 April 1988 Insp Repts 50-254/88-04 & 50-265/88-04 on 880207-0402. Violations Noted.Major Areas Inspected:Operations,Maint, Surveillance,Ler Review,Routine Repts,Temporary Instructions & Administrative Controls Affecting Quality IR 05000254/19880061988-03-31031 March 1988 Insp Repts 50-254/88-06 & 50-265/88-07 on 880315-17.No Violations Noted.Major Areas Inspected:Licensee Actions on Previously Identified Items,Emergency Plan Activations, Review of Licensee Initiatives to Improve Program IR 05000254/19870331988-02-24024 February 1988 Insp Repts 50-254/87-33 & 50-265/87-33 on 871206-880206. Violations & Deviations Noted.Major Areas Inspected: Operations,Maint & Surveillance,Ler Review,Routine Repts & Administrative Controls Affecting Radiation Control IR 05000254/19880031988-02-0404 February 1988 Partially Withheld Physical Security Insp Repts 50-254/88-03 50-265/88-03 on 880111-14 (Ref 10CFR73.21).No Violations Noted.Major Areas Inspected:Mgt Effectiveness Security Program Audits,Records & Repts 1990-08-22
[Table view] Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS
MONTHYEARIR 05000254/19990171999-09-15015 September 1999 Insp Repts 50-254/99-17 & 50-265/99-17 on 990823-27.No Violations Noted.Major Areas Inspected:Pilot Baseline Insp for Annual Review of Changes to Safety Analysis Rept & Biennial Review Permanent Plant Mod IR 05000254/19990151999-08-25025 August 1999 Insp Repts 50-254/99-15 & 50-265/99-15 on 990816-20.No Violations Noted.Major Areas Inspected:Maint Rule Implementation IR 05000254/19990101999-08-20020 August 1999 Insp Repts 50-254/99-10,50-265/99-10,50-454/99-09, 50-455/99-09,50-456/99-10 & 50-457/99-10 on 990628-0721. Major Areas Inspected:Licensee C/A Approach & Implementation of Configuration Control Processes at Each Site IR 05000254/19990161999-08-19019 August 1999 Insp Repts 50-254/99-16 & 50-265/99-16 on 990719-22. Violations Noted.Major Areas Inspected:Physical Protection Cornerstone,Including Review of Access Authoization Program & Changes to Security Plan IR 05000254/19990121999-08-13013 August 1999 Insp Repts 50-254/99-12 & 50-265/99-12 on 990628-0716. Violations Noted.Major Areas Inspected:Corrective Action Process Which Included Methods Used for Identification, Cause Investigation & Correction of Quality Related Items IR 05000254/19990111999-08-13013 August 1999 Insp Repts 50-254/99-11 & 50-265/99-11 on 990601-0720.NCVs Noted.Major Areas Inspected:Performance in Initiating Events,Mitigating Sys,Barrier Integrity Cornerstones & Performance Indicator Verification IR 05000254/19990141999-07-30030 July 1999 Insp Repts 50-254/99-14 & 50-265/99-14 on 990713-15.One Violation Noted & Treated as Ncv.Major Areas Inspected: Heat Sink Performance,Which Covers Inspectable Area Under Initiating Events & Mitigation Sys IR 05000254/19990131999-07-29029 July 1999 Insp Repts 50-254/99-13 & 50-265/99-13 on 990628-0702.No Violations Noted.Major Areas Inspected:Public Radiation Safety & Review of Gaseous & Liquid Radiological Effluents & of Radiological Environmental Monitoring Program IR 05000254/19990091999-06-23023 June 1999 Insp Repts 50-254/99-09 & 50-265/99-09 on 990421-0531.One Violation of NRC Requirements Occurred & Being Treated as non-cited Violation.Major Areas Inspected:Aspects of Licensee Operations,Engineering,Maint & Plant Support IR 05000254/19990061999-05-14014 May 1999 Insp Repts 50-254/99-06 & 50-265/99-06 on 990307-0420.Three Violations Noted & Being Treated as non-cited Violations. Major Areas Insptected:Aspects of Licensee Operations,Maint, Engineering & Plant Support IR 05000254/19990081999-05-11011 May 1999 Insp Repts 50-254/99-08 & 50-265/99-08 on 990419-23.No Violations Noted.Major Areas Inspected:Adequacy of Licensee Programs,Procedures,Training & Supporting Documentation IR 05000254/19990031999-04-0909 April 1999 Insp Repts 50-254/99-03 & 50-265/99-03 on 990308-12.No Violations Noted.Major Areas Inspected:Maint & Engineering IR 05000254/19990011999-04-0101 April 1999 Insp Repts 50-254/99-01 & 50-265/99-01 on 990121-0306. Violations Noted.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support IR 05000254/19990071999-03-31031 March 1999 Radiation Protection Insp Repts 50-254/99-07 & 50-265/99-07 on 990309-12.No Violations Noted.Major Areas Inspected:Solid Radwaste Processing & Control Program & Radioactive Matls Shipping Program IR 05000254/19980211999-03-0505 March 1999 Insp Repts 50-254/98-21 & 50-265/98-21 on 981112-1218. Violation Noted:Major Areas Inspected:Isi Activities at Plant During Refueling Outage 15 ML20207G1771999-03-0505 March 1999 Notice of Violation from Insp on 99112-1218.Violation Noted:Licensee Had Not Included in Revised ISI Program,Basis for Determination That Code Required Exam Was Impractical For,Unit 2 Reactor Pressure Vessel Nozzle Weld Nsb IR 05000254/19990041999-02-26026 February 1999 Insp Repts 50-254/99-04 & 50-265/99-04 on 990201-05.No Violations Noted.Major Areas Inspected:Emergency Prepardeness Program as Aspect of Plant Support IR 05000254/19990021999-02-25025 February 1999 Insp Repts 50-254/99-02 & 50-265/99-02 on 990125-29.No Violations Noted.Major Areas Inspected:Radiation Protection & Chemistry Program Included Water Chemistry Control, Instrument Quality Control & internal-lab Comparison IR 05000254/19980241999-01-14014 January 1999 Partially Withheld Security Insp Repts 50-254/98-24 & 50-265/98-24.Violations Noted.Major Areas Inspected:Plant Support Activities Re Physical Protection of Quad Cities Facility.Details Withheld (Ref 10CFR2.790) IR 05000254/19980221998-12-28028 December 1998 Insp Repts 50-254/98-22 & 50-265/98-22 on 981130-1204.No Violations Noted.Major Areas Inspected:Radiation Protection Staff Preparation for Q1R15 Refueling Outage,Including Review of ALARA Planning & Work Plan Integration IR 05000254/19980201998-12-28028 December 1998 Insp Repts 50-254/98-20 & 50-265/98-20 on 981014-1201.No Violations Noted.Major Areas Inspected:Operations,Maint & Plant Support IR 05000254/19980191998-12-18018 December 1998 Insp Repts 50-254/98-19 & 50-265/98-19 on 981019-1106. Violations Noted.Major Areas Inspected:Effectiveness of Engineering & Technical Support Provided to Plant in Performance of Routine & Reactive Site Activities ML20198G2901998-12-18018 December 1998 Notice of Violations from Insp on 981019-1106.Violations Noted:As of 980327,performance of Listed Test Procedures Did Not Demonstrate Equipment Could Perform Satisfactorily Under Design Conditions IR 05000254/19980171998-11-0505 November 1998 Insp Repts 50-254/98-17 & 50-265/98-17 on 980902-1014.No Violations Noted.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support IR 05000254/19980181998-10-15015 October 1998 Partially Withheld Insp Repts 50-254/98-18 & 50-265/98-18 on 980914-18 (Ref 10CFR73.71).No Violations Identified.Major Areas Inspected:Review of Plant Support Activities,Security Activities Re Onsite Personnel Access & Communications IR 05000254/19980131998-09-22022 September 1998 Insp Repts 50-254/98-13 & 50-265/98-13 on 980716-0901.No Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000254/19980141998-09-17017 September 1998 Insp Repts 50-254/98-14 & 50-265/98-14 on 980825-28.No Violations Noted.Major Areas Inspected:Evaluation of Licensee Performance During Plant Biennial Exercise of Emergency Plan ML20154G4301998-09-11011 September 1998 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $88,000.Violation Noted:As of 970926,licensee Failed to Provide Alternate Shutdown Capability for Some Fire Areas of Facility Containing Safe Shutdown Equipment ML20195D1951998-09-0808 September 1998 EN-98-057B:on 980911,notice of Proposed Imposition of Civil Penalty in Amount of $88,000 Issued to Licensee.Action Based on One Severity Level II Problem Involving Very Significant Inadequacies in Comm Ed Capability to Shut Down IR 05000254/19980161998-09-0404 September 1998 Insp Repts 50-254/98-16 & 50-265/98-16 on 980810-14.No Violations Noted.Major Areas Inspected:Radiation Protection Program Included External & Internal Exposure Control,Whole Body Counting & Contamination & Survey Monitoring Program ML20195D2341998-08-11011 August 1998 EN-98-057:on 980814,notice of Proposed Imposition of Civil Penalty in Amount of $143,000 Issued to Licensee.Action Based on One Severity Level II Problem & One Severity Level III Violation ML20237D6671998-08-11011 August 1998 Notice of Violation from Insp on 980529-0716.Violation Noted:On 980622,while Performing Quad Cities Operating Surveillance Procedure 6600-01,rev 24,operator Failed to Position Throttle Air Box Drain Valve One Turn IR 05000254/19980151998-07-31031 July 1998 Insp Repts 50-254/98-15 & 50-265/98-15 on 980721-24.No Violations Noted.Major Areas Inspected:Aspects of Licensee Corrective Actions & Engineering Involvement in Corrective Actions Process IR 05000254/19980111998-07-0202 July 1998 Insp Repts 50-254/98-11 & 50-265/98-11 on 980504-22. Violations Noted.Major Areas Inspected:Quad Cities Safe Shutdown Analysis & Supporting Procedures ML20236M0831998-07-0202 July 1998 Notice of Violation from Insp on 980401-0529.Violation Noted:On 980501,Interim Procedure 98-0035 Was Not Implemented When Change Was Made to Personnel Out-of Svc Number 98-512 Which Was Not Reviewed & Approved ML20248L7951998-06-0505 June 1998 Notice of Violation from Investigation on 970530.Violations Noted:Licensee Provided to Commission on 960825,operability Determination Checklist.Info Inaccurate Because Supporting Calculations Showed FICs to Be Excess of 1.0 ML20237E7051998-06-0505 June 1998 EN-98-043:informs Commission That Staff Intends to Exercise Enforcement Discretion Per Section VI.B.6 of Enforcement Policy & Not Issue NOV to Util for Failure to Provide Complete & Accurate Info to NRC ML20247P4551998-05-15015 May 1998 Notice of Violation from Insp on 971014-980415.Violation Noted:On 971215,inspector Identified That Licensee Failed to Provide Training of Personnel Performing Activities Affecting Quality IR 05000254/19980081998-05-11011 May 1998 Insp Repts 50-254/98-08 & 50-265/98-08 on 980407-09 & 14-17. No Violations Noted.Major Areas Inspected:Maint,Quality Assurance & Engineering IR 05000254/19980101998-05-0606 May 1998 Insp Repts 50-254/98-10 & 50-265/98-10 on 980413-17.No Violations Noted.Major Areas Inspected:Liquid & Gaseous Effluent Programs,Annual Effluent Rept,Continuous Air & Area Radiation Monitors IR 05000254/19982011998-05-0606 May 1998 Insp Repts 50-254/98-201 & 50-265/98-201 on 980216-0327.No Violations Noted.Major Areas Inspected:Evaluation of Capability of Selected Sys to Perform Safety Functions Required by Design Bases ML20217G3401998-04-23023 April 1998 Insp Repts 50-254/98-04 & 50-265/98-04 on 980211-0331. Violations Noted.Major Areas Inspected:Operations, Engineering,Maint & Plant Support ML20217G2341998-04-23023 April 1998 Notice of Violation from Insp on 980216-0326.Violation Noted:Between 971006 & 10,work Package 970104149-03 Replaced 2A Recirculation Loop Sample Pci Valve AO-2-0220-44,activity Affecting Quality,Prepared & Installed Prior to 971014 ML20217G3101998-04-23023 April 1998 Notice of Violations from Insp on 980211-0331.Violations Noted:On 980314,non-licensed Operators Performing Plant Operating Procedure 6600-7,rev 6,attachment H,Failed to Charge Breaker Closing Spring for Unit 2 IR 05000254/19980051998-04-23023 April 1998 Insp Repts 50-254/98-05 & 50-265/98-05 on 980216-0326. Violations Noted.Major Areas Inspected:Engineering,Including Allowances for Development of Emergency & Immediate Mods IR 05000254/19980071998-04-22022 April 1998 Insp Repts 50-254/98-07 & 50-265/98-07 on 980330-0403.No Violations Noted.Major Areas Inspected:Plant Support Activities Re Physical Protection of Plant,Adequacy of Security Procedures & Event Logs IR 05000254/19983031998-04-13013 April 1998 Exam Repts 50-254/98-303OL & 50-265/98-303OL on 980316-20. Exam Results:All Three Applicants Passed All Portions of Respective Exams ML20217D9661998-03-0909 March 1998 EN-98-010:informs That NOV & Proposed Imposition of Civil Penalty in Amount of $330,000 Will Be Issued on or About 980312 to Comm Ed.Action Based on Two Severity Level III Problems Consisting of Violations ML20216C2531998-03-0606 March 1998 Notice of Violation from Insp on 971224-980210.Violation Noted:From 971216-20,both Standby Gas Treatment Subsystems Inoperable & Unit 1 Remained in Mode 1 & Not Placed in Hot Shutdown Condition within 12 H ML20216C2601998-03-0606 March 1998 Insp Repts 50-254/97-28 & 50-265/97-28 on 971224-980210. Violations Noted.Major Areas Inspected:Operations,Maint & Engineering 1999-09-15
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U.S. NUCLEAR REGULATORY COMMISSION
REGION III
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Reports No. 50-254/89028(DRP);50-265/89028(DRP)
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Docket Nos. 50-254, 50-265 Licenses No. DPR-29; DPR-30
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Licensee: Comonwealth Edison Company L
Post Office Box 767 Chicago, IL 60690 j
Facility Name: Quad Cities Nuclear Power Station, Units I and 2
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Inspection At: Quad Cities Site, Cordova, Illinois
Inspection Conducted: December 17, 1989 through January 27, IM
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i Inspectors:
R. L. Higgins J. M. Shine R. Bocanegra
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Approved
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seactor Projects Section IB Date
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Inspection Summary
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L Inspection on December 17.1989 throu 3h January 27. 1990 (Reports
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L No. 50-254/89028(DRP); 50-265/B9028(DTP))
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Areas Inspected: Routine, unannounced safety inspection by the resident and l
regional inspectors of licensee actions on previous items, plant operations:
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radiological controls, maintenance / surveillance, emergency preparedness,
I security, engineering / technical support and safety assessment / quality
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l Results: During the inspection period, one violation involving improper procedure review was noted (refer to Paragraph 9.a), but since it satisfied the five criteria of 10 CFR Part 2, Appendix C, no Notice of Violation will
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be issued. Other than this violation, licensee
)erformance was good, especially
in the areas of maintenance and operations. A s1 ort outage was taken on each unit, and both outages were completed on schedule with no complications or
errors.
Unit I was shutdown to plug leaking condenser tubes in order to maintain reactor water purity far in excess of that required by Technical i
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Specifications. Unit 2 experienced an abnormally high drywell floor drain sump leakage rate, and this parameter was given enhanced scrutiny by the licensee.
As soon as the leakage rate approached the Technical Specification limit, Unit 2 was promptly shutdown and the leaking components repaired.
9002260346 900213
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PDR ADOCK 05000254 :
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DETAILS 1.
Personnel Contacted l
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- R. Robey, Technical Superintendent
- R. Hopkins, Quality Assurance
- T. Barber, Regulatory Assurance
- Denotes those present at the exit interview on January 29, 1990.
The inspectors also contacted and interviewed other licensee and contractor personnel during the course of this inspection.
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2.
Action on Previous Items (92701 and 92702)
Open items a.
(Closed)OpenItem 254/89026-02: Untested Local Leak Rate Test (LLRT) Volumes.
This issue is addressed by LER 254/90001 and is discussed in Paragraph 9.b.(7) of this report. This item is considered closed.
b.
_(Closed)OpenItem 265/89026-04:
HPCI Deluge and HPCI Steam Isolation.
This issue is addressed by lER 265/90001 and is discussed in Paragraph 9.b.(8) of this report. This item is considered closed.
3.
PjantOperations(71707)
The inspectors, through direct observation, discussions with licensee personnel, and review of applicable records and logs, examined plant operations. The inspectors verified that all activities were accomplished in a tinely manner using approved procedures and drawings and were inspected / reviewed as applicable; and that procedures, procedure revisions and routine reports were in accordance with Technical Specifications, regulatory guides, and industry codes or standards. Additionally, the inspectors verified that approvals were obtained prior to initiating any work; activities were accomplished by qualified personnel; the limiting i
conditions for operation were met during normal operation and while components or systems were removed from service; functional testing and/or calibrations were performed prior to returning components or systems to service; and independent verification of equipment lineup and
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review of test results were accomplished. Also verified were quality control records for being properly maintained and reviewed, and parts, materials and equipment for proper certification, calibration, storage, and maintenance as applicable. The inspectors conducted frequent tours of plant facilities to observe any adverse plant conditions such as equipment malfunctions, potential fire hazards, radiological hazards, s
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fluid leaks, excessive vibrations, and personnel errors. The inspectors'
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review ensured that any such issues were addressed in a timely manner with sufficient and proper corrective actions and reviewed by appropriate management personnel, a.
Engineered Safety Features System Walkdown (71710)
During plant tours of Units 1 and 2, the inspectors walked down some of the accessible portions of the High Pressure Coolant Injection (HPCI),ReactorCoreIsolationCooling(RCIC),CoreSpray (CS), Residual Heat Removal (RHR), RHR Service Water, Standby Liquid Control (SLC) Systems, and Standby Gas Treatment (SGT) Systems. The inspectors also walked down the Emergency Diesel Generators (EDG)
and the Station Batteries. No violations or deviations were noted, b.
Sumary of Operations
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Unit 1 Unit 1 operated at power until it was shutdown on January 20,(3) of
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1990,
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to plug leaking main condenser tubes (refer to paragraph 3.c.
thisreport). Unit I restarted on January 21, 1990, and operated at power throughout the inspection period.
Unit 2
Unit 2operatedatpoweruntilitwasshutdownonJanuary)13ofthis 1990, to repair leaks in the drywell (refer to Paragraph 3.c.(1
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report).
Unit 2 restarted on January 14, 1990, and operated at power throughout the remainder of the inspection period.
c.
Onsite followup of Events at Operating Power Reactors (93702)
(1) Unit 2 Shutdown and Startup
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On January 13,1990, Unit 2 was shutdown because drywell floor drain sump leakage had increased from 3.3 gpm to 4.0 gpm (the TechnicalSpecificationlimitis5.0gpm).
Repairs were made to the 2-220-58A feedwater check valve (seal ring leak), the
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2-1402-6B core spray valve (seal ring leak), and to the L
2-263-2-398 jet pump instrumentation tap drain isolation valve (packing leak). Unit 2 restarted on January 14, and l
I was reconnected to the electrical grid on January 15, 1990.
After startup, the drywell floor drain sump leakage equalized at 3.7 gpm due to a packing leak on the inboard RCIC containment isolationvalve(2-1301-16). The monitoring frequency for
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drywell floor drain sump leakage has been increased from every four hours to every two hours, and contingency plans have been made to shutdown should the leakage rate approach the Technical Specification limit.
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(2) Unit IC Reactor Feedpump Leak On January 17, 1990, with Unit I near full power, an unisolable through wall leak developed on the IC reactor feed Jump. Since the 1A reactor feed pump was out of service, only tie IB reactor feed pump was available. A rapid power reduction to 50% power was made in order to stay within the capacity of one reactor feed pump. On January 15, 1990, the IC reactor feed pump was repaired and returned to service, and Unit I was returned to full power.
(3) Unit 1 Shutdown and Startup On January 20, 1990, Unit I was shutdown in order to pluo leaking tubes in the main condenser (reactor water conductivity had increased over a one month period from its normal value of
.08 micrombos/cm to.2 micrombos/cm; the Technical Specification limit is 10 micrombos/cm), repair leaks on the "B" and "C" electromatic relief valves, and perform other minor maintenance.
Unit I restarted on January 21, and was reconnected to the electrical grid on January 22, 1990.
4.
RadiologicalControls(71707)
Observations by the inspectors indicated that the licensee's performance in the area of radiological controls was good. Management remains connitted to an aggressive ALARA program.
Personnel exposure has been higher than budgeted during the inspection period because of an unforeseen outage on each unit.
5.
Maintenance / Surveillance a.
Monthly Maintenance Observation (62703)
Station maintenance activities of safety-related and nonsafety-related systems and components listed below were observed / reviewed to ascertain that they were conducted in accordance with approved procedures, regulatory guides and industry codes or standards and in conformance with Technical Specifications.
The following items were considered during this review:
the limiting conditions for operation were met while components or systems were removed from service; approvals were obtained prior to initiating the work; activities were accomplished using approved procedures and were inspected as applicable. Additional items reviewed included verification that functional testing and/or calibrations were performed prior to returning components or systems to service; quality control records were maintained; and activities were accomplished by qualified personnel. Also,.the inspectors verified that parts and materials used were properly certified; radiological controls were implenented; and fire prevention procedures were followed. Work requests were reviewed to determine the status
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of outstanding jobs and to assure that priority is assigned to the maintenance of safety related equipment which may affect system performance.
Portions of the following activit_1es were observed / reviewed:
(1) Painting and labeling of alant coinponents.
(2) Backseating the Unit 2 in>oard RCIC containment isolation valve.
No violations were identified in this area, b.
Monthly Surveillance Observation (61726)
The inspectors observed surveillance testing required by the Technical Specification and verified that testing was performed in accordance with adequate procedures, that test instrumentation was calibrated, and that limiting conditions for operation were met. Additionally, the inspectors observed / verified the removal and restoration of the affected components, and that test results conformed with Technical Specifications and procedure requirements. Also, the inspectors verified that the results were reviewed by personnel other than the individual directing the test and that any deficiencies identified during the testing were properly reviewed and resolved by appropriate management personnel.
Portions of the following activities were observed / reviewed:
New fuel receipt inspection.
Shipment damaged unirradiated fuel.
Unit 2 RCIC steam supply isolation valves operability test.
No violations or deviations were identified in this area.
6.
Emergency Preparedness (71707)
During the inspection period, the Resident Inspectors inspected the Quad Cities Technical Support Center (TSC) and monitored a test of-the Emergency Notification System (ENS) phone.
No violations or deviations were noted.
7.
Securit.y (71707)
During the inspection period, the ins)ectors toured the plant and the Central Alarm Station to assure t1at security programs were being j
properly implemented. The inspectors verified that security barriers were in place, security doors were operable, the security force was alert, personnel correctly displayed their identification badges and visitor access was being properly controlled. During the inspection period, the licensee implemented a more rigorous procedure for issuing badges to personnel in the ate house to ensure that station personnel do not get issued someone e se's badge.
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No violations or deviations were noted.
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Engineering / Technical Support Installation and Testing of Modifications (37828)
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The feedwater hydrogen addition modification for both units is continuing.
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The feedwater hydrogen addition modification for Unit 2 will not be
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completed prior to the Unit 2 outage due to a combination of engineering
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problems and management priorities.
9.
Safety Assessment / Quality Verification
a.
Evaluation of Licensee Quality Assurance Program Implemer.tation (35502)
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During the inspection period, the inspectors met frequently with
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members of the licensee's Quality Assurance staff to discuss the
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licensee's Quality Assurance program.
The inspectors also monitored Quality Assurance and Quality Control personnel auditing the
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backseating of the Unit 2 inboard RCIC containment isolation valve.
Improper Procedure Review On December 19, 1989, the licensee discovered QAP 1100-7 Approval
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and Authorization of Temporary Procedures and Temporary Changes to Permanent Procedures, to be in violation of Technical Specification
(TS) 6.2.C.1 for Temporary Procedure Changes involving a change in intent. QAP 1100-7 did not require signatures from both the Department Head and Assistant Superintendent as stated in Technical
Specification 6.2.C.1.
This is considered to be a Severity Level IV violation (254/89028-02).
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The cause of this event was management oversight in the preparation
and review of a previous change to Technical Specification 6.2.C.I.
The change mistakenly added the Assistant Superintendent in the review process when the intent was only to replace the Department
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Head Review.
l QAP 1100-7, and the associated procedures, QAP 1100-7-T1 and T6, have been revised to comply with Technical Specification 6.2.C.1.
Because this violation satisfied the criteria of 10 CFR 2, Appendix C Section V.G (it was licensee-identified, was promptly reported and corrected, was Severity Level IV or V, and could not g
have been prevented by the licensee's corrective action for a f
previous violation) no Notice of Violation will be issued. This item is considered closed, i
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In-Office Review of Written Reports of Nonroutine Events at Power Reactor Facilities (90712) and Onstte Followup of Written Reports
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of Nonroutine Events at Power Reactor Facilities (92/00)
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During the inspection period, the resident ir.spectors reviewed incidents such as scrams, ESF actuations and component failures
which occurred at other plants. The resident inspectors informed the licensee of the details of all events which potentially had
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applicability to components or activities at Quad Cities.
LER Review L
(1)
(0 pen)LER 265/89020, Revision 01: ECCS Initiation Due to Valving Error.
ThisrevisionupdatestheoriginalLER(discussedinInspection Reports No. 254/88029; 265/88029) by specifying the corrective
actions which the licensee commits to implement.
This LER will remain open pending the implementation of the specified
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corrective actions.
(2) (Closad)LER 254/89021, Revision 00:
HPCI Fire Protection
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Technical specification Surveillance Functional Test Not Completed on Time.
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This event is discussed in Paragraph 6.b.(3) of Inspection
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Report No. 254/89026. All event-specific corrective actions
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have been completed.
This LER is considered closed.
(3)
(0 pen)LER 254/89022, Revision 00: Unit 1 HPCI Inoperable Due to Inadvertent Deluge System Actuation.
Thisevent.isdiscussedinParagraph3.c.(5)ofInspection i
Report No. 254/89025.
It will remain open pending the f
installation of a preaction system to replace the current
fire nozzles.
(4)
(0 pen)LER 254/89023, Revision 00:
Violation of Technical Specifications Concerning Review of Temporary Procedures.
This event is discussed in Paragraph 9.a. of this report.
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(1) The revision of Technical Specification 6.2.C.1 to replace the Department Head with the Assistant Superintendent in the procedure review process; and
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(2) The imalementation of a procedure to review procedures when a Tec1nical Specification change is implemented.
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(0 pen) LER 254/89025, Revision 00: Potential Damage to New (
Fuel Bundle From Impact of Reactor Building Crane Auxiliary l-Hook.
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On December 14, 1989, the reactor building overhead crane auxiliary hoist was accidentally lowered onto new fuel bundle
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LYU325 during fuel receiving activities. On December 20, 1989, the licensee determined that damage to the new fuel bundle may exceed $2,000.00.
The cause of this event was personnel error involving an c
inadvertent action due to inattention. The fuel handler operating the overhead crane lowered the hoist without a signal man and inadvertently continued to lower the hoist until the hook had contacted the fuel bundle.
Corrective action included temporarily removing the fuel handler from operating the crane. The fuel bundle was shipped back to General Electric for inspection and replacement of any possibly damaged parts. This LER will remain open pending further review of the procedures for crane operation, heavy load movement and lifting and rigging.
(6) _(Open)LER_254/89026 Revision 00: Control Room HVAC Isolation Due to Dried Out Chlorine Probe.
On December 25, 1989, a High Chlorine Concentration signal was noted on the Toxic Gas Monitoring portion of the Control Room Heating, Ventilation, and Air Conditioning System. This resulted in a Control Room HVAC Engineered Safety Feature (ESF). A four hour Emer0ency Notification System (ENS) Phone Notification was made in accordance with 10 CFR 50.72(b)(2)(11).
On December 26, 1989, the monitor's chlorine analyzer probe was injected with an electrolytic solution in accordance with QlP 5700-2, Filling Procedure for the Chlorine Analyzer Probe.
On December 27, 1989, the chlorine circuit of the Toxic Gas Analyzer was calibrated in accordance with QIS 79-51, Gas Analyzer Calibration and Functional Test Data Sheet, and the system was returned to normal operating mode.
The apparent cause of the event was a drying out of the chlorine probe which resulted in a false reading. This event was determined to be an isolated incident, however, the inspection of the' electrolyte level during cold, dry weather will be increased.
This LER will remain open pending the revision of QIP 5700-2 to increase surveillance requirements to weekly intervals during the months of November through March.
(7) _(Open)LER 254/9000). Revision 00: Additional valves added to Local Leak Rate Testing Program due to Self Assessment i
Audit (Voluntary LER).
A licensee study to improve the Type B and C Local Leak Rate Testing (LLRT) Program at Quad Cities Station concluded that seven pathways should be added to the LLRT Program (refer to Paragraph 6.b.(1) of Inspection Reports No. 254/89026; 265/89026). These test volumes included: The Reactor l
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Building Closed Cooling Water (RBCCW) inlet / outlet; the Core Spray Discharge lines; the Instrument Air to the Drywell; the Service Air to the Drywell; the Standby Liquid Control System;
the Clean Demineralized Water to the Drywell; and the Drywell Air Sampling lines. These pathways were excluded from the licensee's LLRT Program due to an interpretation of 10 CFR 50
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Appendix J which did not consider these test volumes applicable to the Type C testing requirements. Due to a recent interpretation of 10 CFR 50 Appendix J with respect to licensing design criteria, these volumes shall be added to the licensee's Type B and C LLRT program. Modification of the systems will be performed as necessary to install the required vents and test taps to perform the Type C testing.
This LER will remain open pending the implementation of its corrective actions.
(8) (0 pen)LER 265/90001 Revision 00:
Unit 2 HPCI Fire Protection Out of Service Greater Than 14 Days.
On December 25, 1989, the number of days the High Pressure Coolant Injection (HPCI) Fire Protection Deluge System had been inoperable exceeded the 14-day reporting requirement of Technical Specification 3.12.C.4.
The HPCI fire Protection Deluge System had conservatively been declared inoperable on December 11, 1989 with it was decided that the function of the steam leak detection high temperature, Group IV, isolation of the HPCI turbine may be delayed (refer to Paragraph 3.c.(5) of Inspection Reports No. 254/89026; 265/89026). A fire watch was initiated in accordance with Technical Specification 3.12.C.3.
The cause of this event is a result of conservative action due to the possibility of the actuation delay of the steam leak detection.
As part of the corrective actions, the HPCI. Fire Suppression System will remain inoperable until a modification is installed to correct the problem.
In the interim, the fire watch frequency has been increased and a temporary procedure has been written on how to manually operate the fire suppression system.
This LER will remain open 1ending the implementation of Modification M4-2-84-21A W11ch will reduce the steam leak isolation setpoint from 185 degrees Fahrenheit to 155 degrees Fahrenheit, c.
Evaluation of Licensee Self-Assessment Capability (40500)
During the inspection period, the inspectors attended a procedure upgrade meeting and an Onsite Review Committee meeting. Both meetings were properly staffed and conducted in a professional manner.
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The inspectors also attended the exit meeting of the corporate Performance Assessment Department's Maintenance Assessment Team.
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The meeting was business-like and the team's findings were
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well-received by station management. Among the more significant
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findings were problems in the areas of System Engineer training,
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maintenance scheduling, work package detail and the use of maintenance programs by ENC.
One violation was identified, but since it satisfied the criteria of
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10 CFR 2, Appendix C, Stction V.G no Notice of Violation will be issued.
10. Management Meetings - Entrance and Exit Interviews (30703)
The inspectors met with licensee representatives (denoted in paragraph 1)
throughout the inspection period and at the conclusion of the inspection
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on January 29, 1990, and summarized the scope and findings of the
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inspection activities, e
The inspectors also discussed the likely informational content of the inspection report with regard to documents or processes reviewed by the inspectors during the' inspection. The licensee did not identify any such
documents / processes as proprietary.
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