IR 05000254/2023001

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Integrated Report 05000254/2023001 and 05000265/2023001
ML23128A101
Person / Time
Site: Quad Cities  Constellation icon.png
Issue date: 05/08/2023
From: Robert Ruiz
NRC/RGN-III/DORS/RPB1
To: Rhoades D
Constellation Energy Generation, Constellation Nuclear
References
IR 2023001
Download: ML23128A101 (1)


Text

May 8, 2023

SUBJECT:

QUAD CITIES NUCLEAR POWER STATION - INTEGRATED INSPECTION REPORT 05000254/2023001 AND 05000265/2023001

Dear David Rhoades:

On March 31, 2023, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Quad Cities Nuclear Power Station. On April 25, 2023, the NRC inspectors discussed the results of this inspection with Brian Wake, Site Vice President, and other members of your staff.

The results of this inspection are documented in the enclosed report.

One finding of very low safety significance (Green) is documented in this report. This finding involved a violation of NRC requirements. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; the Director, Office of Enforcement; and the NRC Resident Inspector at Quad Cities Nuclear Power Station.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; and the NRC Resident Inspector at Quad Cities Nuclear Power Station. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Signed by Ruiz, Robert on 05/08/23 Robert Ruiz, Chief Reactor Projects Branch 1 Division of Operating Reactor Safety Docket Nos. 05000254 and 05000265 License Nos. DPR-29 and DPR-30

Enclosure:

As stated

Inspection Report

Docket Numbers: 05000254 and 05000265 License Numbers: DPR-29 and DPR-30 Report Numbers: 05000254/2023001 and 05000265/2023001 Enterprise Identifier: I-2023-001-0066 Licensee: Constellation Nuclear Facility: Quad Cities Nuclear Power Station Location: Cordova, IL Inspection Dates: January 01, 2023 to March 31, 2023 Inspectors: Z. Coffman, Resident Inspector C. Hunt, Senior Resident Inspector C. Mathews, Illinois Emergency Management Agency L. Rodriguez, Senior Reactor Inspector A. Tran, Resident Inspector Approved By: Robert Ruiz, Chief Reactor Projects Branch 1 Division of Operating Reactor Safety Enclosure

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Quad Cities Nuclear Power Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Inadequate Procedure for Feedwater System Failure Cornerstone Significance Cross-Cutting Report Aspect Section Initiating Events Green [H.14] - 71152A NCV 05000254,05000265/2023001-01 Conservative Open/Closed Bias The inspectors identified a finding of very low safety significance (Green) and an associated non-cited violation (NCV) of Technical Specification 5.4.1, "Procedures," for the licensee's failure to have station procedures appropriate for the circumstances to address a failure of the 2B feedwater regulating valve (FRV) in the full open position. As a result, on November 4, 2022, following a failure of the 2B FRV in the full open position, operators were required to insert a manual trip of the reactor on high water level when they could not arrest the subsequent reactor water level transient. The overfeed condition was due to a latent design vulnerability in the 2B FRV allowing it to be capable of passing greater than 100 percent total feedwater flow at full reactor power.

Additional Tracking Items

Type Issue Number Title Report Section Status LER 05000265/22-003-00 LER 022-003-00 for Quad 71152A Closed Cities Nuclear Power Station, Unit 2, Manual Scram Due to Feedwater Regulator Valve Failure Increasing Reactor Water Level

PLANT STATUS

Unit 1 The unit began the inspection period at full-rated thermal power. On January 20, 2023, the unit began its end-of-cycle coastdown period. The unit shut down on March 26, 2023, for refueling outage Q1R27 and remained in a shutdown condition through the end of the inspection period.

For all other periods, the unit was at full-rated thermal power with the exception of short-term power reductions for control rod sequence exchanges, testing, and as requested by the transmission system operator.

Unit 2 The unit began the inspection period at full-rated thermal power. On January 21, 2023, the unit was down powered to approximately 70 percent to perform maintenance on the 2B feedwater regulating valve. The unit was returned to full-rated thermal power on January 22, 2023, where it remained with the exception of short-term power reductions for control rod sequence exchanges, testing, and as requested by the transmission system operator.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Impending Severe Weather Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated the adequacy of the overall preparations to protect risk-significant systems from impending severe weather (high winds, thunderstorms, and tornado watch/warning) on March 31, 2023.

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) 1A residual heat removal (RHR) on February 8, 2023
(2) 1C RHR on February 16, 2023
(3) Unit 1 reactor core isolation cooling (RCIC) on February 27, 2023
(4) Unit 1 high-pressure coolant injection (HPCI) following planned maintenance window on March 1, 2023

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (6 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1) Fire Zone (FZ) 8.2.7.A, Unit 1 turbine building (TB), elevation 615'-6", hydrogen seal oil area and motor control centers on January 4, 2023
(2) FZs 6.1.A and 6.1.B, Unit 1 TB, elevation 615'-6", 'A' and 'B' battery charger room on February 2, 2023
(3) FZs 6.2.A and 6.2.B, Unit 2 TB, elevation 615'-6", 'A' and 'B' battery charger room on February 17, 2023
(4) FZ 11.1.3, Unit 1 reactor building, elevation 554'-0", HPCI and HPCI access tunnel on February 28, 2023
(5) FZ 8.2.7.B, Q1R27 hot work in Unit 2 TB, elevation 615'-6" and 608'-6", low-pressure heater bay (east and west) on March 29, 2023
(6) FZ 8.2.6.A, Unit 1 TB, elevation 595'-0", 'D' heater bay on April 5, 2023

71111.06 - Flood Protection Measures

Flooding Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated internal flooding mitigation protections in the:

Flood Zone 8.2.8.A SWGR [switchgear] area MG [motor generator]

set(s)/elevation 639'/building: TB-U1 on February 2, 2023

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01)

(1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the control room during the Unit 1 reactor shutdown for Q1R27 on March 27, 2023.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated licensed operator requalification exercises in the simulator on February 9, 2023.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (1 Sample)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:

(1) Action Request (AR) 4523962, "Unit 2 EDG [emergency diesel generator] Failed to Start," on September 22, 2022

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) Units 1 and 2 elevated risk due to Unit 2 125 Vdc battery charger load test on January 10, 2023
(2) Unit 2 elevated risk during a planned downpower for feedwater regulating valve repairs on January 20, 2023
(3) E-2 certification meeting and risk management for work week 3/20/2023 on March 9, 2023
(4) Q1R27 shutdown safety plan review on March 24, 2023
(5) Q1R27 shutdown safety reviews and protected equipment walkdowns during week of March, 27, 2023

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (6 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1) 'B' control room emergency ventilation system freeze seal work on January 3, 2023
(2) AR 4542921, "Recommend Unit 2 SBLC [standby liquid control] Heat Trace Replacement," on February 5, 2023
(3) Unit 2 HPCI pump piping connection leaks on February 5, 2023
(4) AR 4558106, "HPCI Signal Converter Motor Gear Unit Drive Signal Issues," on March 1, 2023
(5) AR 4554301, "Unexpected 901-8 A-4 Alarm," for the 1/2 emergency diesel generator on March 2, 2023
(6) Unit 1 HPCI turning gear impact on operability on March 3, 2023

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Partial)

(1) (Partial) Q1R27 refueling outage beginning March 26, 2023 through March 31, 2023

71111.24 - Testing and Maintenance of Equipment Important to Risk

The inspectors evaluated the following testing and maintenance activities to verify system

operability and/or functionality: Post-Maintenance Testing (PMT) (IP Section 03.01)

(1) 1B RHR service water pump comprehensive test on January 18, 2023
(2) Unit 2 EDG after replacement of the air pressure control valve (PCV) 224 valve on March 7, 2023
(3) Unit 1 HPCI PMT after maintenance window on March 2, 2023
(4) Unit 1 1A core spray pump breaker replacement on March 23, 2023

Surveillance Testing (IP Section 03.01) (7 Samples)

(1) Unit 1 EDG monthly load test on January 9, 2023
(2) QCOS 1400-01, "1B Core Spray System Flow Rate Test," on February 13, 2023
(3) QCOS 1000-44, "Unit 2 'B' Loop LPCI [low-pressure coolant injection] and Containment Cooling Modes of RHRS [residual heat removal system] Non-Outage Logic Test," on March 9, 2023
(4) QCIS 1400-01 and QCIS 1400-05, "Unit 2 Core Spray Pump Discharge Flow Trip and Cal Test," on March 9, 2023
(5) QCOS 6500-09, "Function Test of Unit 1 Second Level Undervoltage," on March 13, 2023
(6) QCOS 7500-05, "SBGTS [standby gas treatment system] Operability Test," on March 16, 2023
(7) QCOS 1300-05, "RCIC Pump Operability Test," on March 21, 2023

Inservice Testing (IST) (IP Section 03.01) (3 Samples)

(1) QCOS 1100-07, "SBLC Pump Flow Rate Test," revision 42, for the 2A SBLC pump on February 27, 2023
(2) QCOS 1300-05, "RCIC Pump Operability Test," revision 63, on March 7, 2023
(3) QCOS 1400-05, "Core Spray Pump Flow Rate Test," revision 52, on March 22, 2023

Containment Isolation Valve (CIV) Testing (IP Section 03.01) (1 Sample)

(1) QCOS 0100-11, "HPCI Steam Supply Local Leak Rate Test MO 1(2)-2301-4 MO 1(2)-2301-5," revision 1, on March 28, 2023

Reactor Coolant System Leakage Detection Testing (IP Section 03.01) (1 Sample)

(1) AR 4553630, "U2 DWFDS [drywell floor drain sump] Leakage Increasing Trend," on February 14, 2023

71114.06 - Drill Evaluation

Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01)

(1 Sample)

(1) The inspectors observed activities related to the technical support center during an emergency preparedness drill on February 7, 2023.

Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)

The inspectors evaluated:

(1) Focused emergency preparedness drill on January 31,

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:

IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01) ===

(1) Unit 1 (January 1, 2022, through December 31, 2022)
(2) Unit 2 (January 1, 2022, through December 31, 2022)

IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02)

(2 Samples)

(1) Unit 1 (January 1, 2022, through December 31, 2022)
(2) Unit 2 (January 1, 2022, through December 31, 2022)

IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 02.03) (2 Samples)

(1) Unit 1 (January 1, 2022, through December 31, 2022)
(2) Unit 2 (January 1, 2022, through December 31, 2022)

71152A - Annual Follow-up Problem Identification and Resolution Annual Follow-up of Selected Issues (Section 03.03)

(1) AR 4534873, "Unit 2 Scram on Reactor High Water Level," on March 6, 2023

71153 - Follow-Up of Events and Notices of Enforcement Discretion Event Report (IP section 03.02)

The inspectors evaluated the following licensee event reports (LERs):

(1) LER 265/2022-003-00, "Manual Scream Due to Feedwater Regulator Valve Failure Increasing Reactor Water Level" (ADAMS Accession No. ML22364A273). The inspection conclusions associated with this LER are documented in this report under the Inspection Results Section 71152A. This LER is closed.

INSPECTION RESULTS

Inadequate Procedure for Feedwater System Failure Cornerstone Significance Cross-Cutting Report Aspect Section Initiating Events Green [H.14] - 71152A NCV 05000254,05000265/2023001-01 Conservative Open/Closed Bias The inspectors identified a finding of very low safety significance (Green) and an associated non-cited violation (NCV) of Technical Specification 5.4.1, "Procedures," for the licensee's failure to have station procedures appropriate for the circumstances to address a failure of the 2B feedwater regulating valve (FRV) in the full open position. As a result, on November 4, 2022, following a failure of the 2B FRV in the full open position, operators were required to insert a manual trip of the reactor on high water level when they could not arrest the subsequent reactor water level transient. The overfeed condition was due to a latent design vulnerability in the 2B FRV allowing it to be capable of passing greater than 100 percent total feedwater flow at full reactor power.

Description:

On November 4, 2022, with Unit 2 operating at full power, the 2B FRV, HO 2-0624B, failed in the full open position without a change in demand signal from the digital feedwater level control (DFWLC) system and without any component manipulation from control room operators. This failure caused an unplanned rise in reactor water level. The DFWLC system compensated for the rising reactor water level by automatically shutting the 2A FRV, HO 2-0624A. Control room operators noted that the 2A FRV shut as expected but did not see a corresponding decrease in reactor water level. The control room operators began to shut MO 2-3206-B, the 2B FRV isolation valve, but prior to MO 2-3206-B fully shutting, manual scram criterion of +44 inches reactor water level was reached and operators manually tripped the unit.

DFWLC System Design The DFWLC system is designed to maintain water level in the reactor vessel within a specified range during plant operation by processing inputs from various plant parameters such as reactor water level, steam flow, and feedwater flow. Based on those parameters, the DFWLC system generates signals to adjust the position of two FRVs to maintain reactor water level at the desired level. Both valves are hydraulically operated and set up, or tuned, to operate within the optimal flow characteristics of the valves. Thus, when the demanded flow of the DFWLC system is 100 percent, typically the FRVs are not physically 100 percent full open. An important feature of the DFWLC system is that a lockup signal is generated by the system whenever there is at least a 10 percent difference between the actual position of an FRV and the demanded position lasting for at least 5 seconds. The time delay is meant to prevent spurious lockups from occurring at steady state conditions but short enough to prevent actual system failures from causing major reactor water level transients. When a lockup occurs, an electric signal halts all FRV motion in the position that existed at the time of the lockup. Operators can procedurally reset the lockup and restore a FRV to operation once the cause of a lockup has been investigated and corrected.

In the mid-1990s, the licensee replaced the control units for the FRVs on both units with new hydraulic actuators. During this modification, the existing 2B FRV was installed which had a maximum stroke length of 14 inches. To achieve the desired flow characteristics, the valve was tuned to the feedwater level control system to a maximum stroke length of 12 inches.

The inspectors noted that these physical characteristics of the valve were not recorded in the design modification package. Additionally, the inspectors were not able to determine if the site performed an evaluation at the time of the modification to assess the risk associated with the valve having the ability to pass significantly more flow than required should certain feedwater level control system failures occur. The inspectors noted that the licensee specifically highlighted the unique physical characteristics of the valve in QDC-3200-M-1491, Hydraulic Analysis of Condensate and Feedwater Systems for EPU Marin Recovery, revision 0, which was performed in 2006, indicating that the licensee was aware of the difference between the 2B FRV and the other FRVs at the site.

External and Internal Operating Experience On March 8, 2019, the licensee issued Nuclear Event Report (NER) NC-19-002-Y, Feedwater Regulating Valve Fleetwide Issues, revision 0, to the fleet. The NER was written to address the fleet actions necessary to improve performance of FRVs to minimize operational risk and to increase the operational reliability of the regulating valve components of the feedwater system. On October 31, 2019, NER NC-19-002-Y, revision 1, was issued which included further actions and additional industry operating experience with FRV failures.

The station completed several actions in response to NC-19-002-Y, including a review of vulnerabilities or enhancements that could be made to harden the system against subcomponent failures and a review of known single point vulnerabilities for the FRVs. The inspectors noted that the hardening review covered various generic mechanical and electrical features of the FRVs but did not specifically perform a review of the design characteristics of the valves. In the sites review of known FRV single point vulnerabilities, the site stated:

Based on the ERVR 2.0 and ERVR 3.0 reviews of the Feedwater (FW) and Feedwater Level Control (FLC) systems, there were no previously identified single point vulnerabilities (SPVs) for the Feedwater Regulating Valves (FRVs). The criterion used during the ERVR reviews for SPVs included equipment that would cause an automatic or manual reactor scram should a failure occur. The FRVs are designed to fail in place, or lockup, should a fault or failure occur.

The site went on to state that one of the original design criterions of the DFWLC system was to be designed with no SPVs. At the time of the response, the site noted that there had been issues with lockups of the FRVs during operation that required maintenance to solve, but those events had not resulted in a plant trip or unplanned shutdown. As such, the sites vulnerability evaluation of the FRVs during follow-on corporate initiatives concluded that the DFWLC system was safe from a single point vulnerability resulting from an electrical or instrumentation and control type failure. Additionally, the site concluded that a mechanical issue with the FRV would likely only result in a downpower of greater than 20 percent to isolate that feedwater line to repair. The inspectors noted that the site did not consider the presence of foreign material adversely affecting FRV operation as a failure mechanism.

Relevant fleet operating experience concerning foreign material obstruction of FRV control was included in NER NC-19-002-Y, revision 1, highlighting a manual reactor scram inserted by operators at the Braidwood station on September 23, 2019 (AR 4281429) due to foreign material found inside the control air portion of the feedwater digital valve controller. This foreign material originated from a manufacturing byproduct internal to the component.

Similarly, on March 21, 2021, operators at the Calvert Cliffs station inserted a manual scram following an FRV failure also due to foreign material originating from the vendor assembly process (AR 4410594).

On May 24, 2021, Quad Cities Unit 1 experienced an issue with the 1B FRV moving from its expected position to full open with no corresponding DFWLC system lockup. Operators attempted to take manual control of the affected valve from the control room but were unsuccessful. Eventually, the valve did lock in place in the full open position. Equipment operators were sent into the field to locally operate the valve with a hydraulic hand pump to return it to the desired position before repairs were ultimately made. Although foreign material was not determined to be the cause of the event, the inspectors noted that this event did illustrate that the DFWLC system lockup feature may not be able to mitigate all failure modes of the FRV in which the valve moves to a full open or shut position before the designed lockup happens.

On July 4, 2022, Quad Cities Unit 2 experienced an unexpected closure of the 2A FRV in which the valve went from its expected position to full shut prior to the DFWLC system lockup occurring. The resulting water level transient ultimately required control room operators to insert a manual scram on low reactor water level. The site performed a root cause investigation under AR 4509196 and determined the cause of the failure was foreign material partially or completely blocking hydraulic flow in the control servo of the FRV. The station was not able to determine the exact origin of the foreign material but believed it to be from either the seal rings used in the assembly of the servo or introduced through the addition of hydraulic oil to the system during maintenance activities. The site performed a risk assessment of the event in accordance with AD-AA-3000, Nuclear Risk Management Process, and created actions to address the specific vulnerabilities identified in the event.

The inspectors noted that no consideration was made to reevaluate the possible failure modes of the FRVs and potential consequences of those failures despite internal and external operating experience, indicating the sites original assumptions regarding the robustness of the DFWLC system may no longer be valid.

On July 12, 2022, Dresden station Unit 2 experienced a failure of the 2A FRV in which the valve went from its expected position to full open. The subsequent transient resulted in an automatic reactor scram. The failure was determined to be due to foreign material introduced during the manufacturing process which interfered with the operation of the valve (AR 4510475).

On August 12, 2022, the licensee corporate office performed a work group evaluation under AR 4511746 in response to the Quad Cities and Dresden FRV events. The evaluation concluded that although the equipment vulnerability reviews performed by Quad Cities and Dresden were consistent with the level of detail provided in operations training and the design basis provided by the vendor, the reviews did not get to the needed depth to understand the full vulnerability of the FRVs. The evaluation determined that operating experience from recent failures and scrams in the industry indicated there was an adverse trend in the failure of pneumatic controllers caused by manufacturing-produced foreign material, but the operating experience was not applied to hydraulic or other feedwater control system designs within the fleet and should have been used as a trigger to perform a deeper review of the fleet FRVs. The evaluation noted that specific discussions during site and corporate challenge boards on the effect of component failures in systems with lockup features, like the one used at Quad Cities, resulted in site responses simply stating that the system will lock up on deviation, loss of air, or hydraulics. The evaluation noted that there were no challenges or discussions with respect to abnormal directional control valve or positioner failures other than the digital system will recognize the deviation and lock the valve in position. Additionally, the evaluation stated that during the challenges it was not recognized that a failure of a single positioner results in an FRV repositioning faster than actuation of the lockup feature at stations such as Quad Cities.

On September 8, 2022, Quad Cities Unit 1 experienced a failure of the 1B FRV in the full open position before it locked up. Operators responded per station procedures and recovered reactor water level. The site performed a work group evaluation on the event under AR 4521360 and determined the cause of the failure was a failed component on the input/output module for the control system. The evaluation determined that with this specific type of failure, the system does not respond to the control system input command and the valve fails full open. The inspectors noted that, although the event was not caused by foreign material, this event illustrated again that the DFWLC lockup feature may not be able to mitigate all failure modes of the FRV in which the valve moves to a full open or shut position before the lockup happens.

2B FRV Failure On November 4, 2022, Quad Cities Unit 2 experienced a failure of the 2B FRV in the full open position and before it locked up. Operators responded in accordance with station procedures and operator training, but unlike the event occurring on Unit 1 on September 8, 2022, operators were not able to compensate for the additional feedwater flow being supplied to the reactor by the 2B FRV even with the 2A FRV fully shut. Control room operators inserted a manual scram as required by station procedures.

The site performed a root cause investigation under AR 4534873 and determined that the cause of the event was due to foreign material that was introduced during the manufacturing or assembly of the 2B FRV control servo. This foreign material interfered with the correct operation of the servo and resulted in a hard over condition which moved the 2B FRV to the fully open position. The site determined that a contributing cause of the event was that the 2B FRV had an excessive valve stroke that was longer than all the other FRVs installed at the site. During initial installation, this was not viewed as an inherent risk because the valve was tuned to only operate over a small portion of its possible valve stroke. The failure observed on November 4, 2022, caused the 2B FRV to move much further in the open direction than was previously believed possible. In the fully open position, the 2B FRV was independently capable of providing more flow than needed for 100 percent power operations. In this condition, closure of the 2A FRV could not have arrested the rising reactor water level trend.

The evaluation additionally stated that the stations operating and abnormal operating procedures lacked any discussion of the 2B FRV's unique construction because the inherent risk of this construction was never recognized during the modification process. Station procedures also lacked any guidance to specifically address a reactor water level transient resulting from a 2B FRV failure in the full open position. Similarly, the work instructions for testing the 2B FRV did not identify that the valve was physically capable of passing more than 100 percent rated flow, as the calibration procedure only calibrated the valve to operate in a normal operating band. The evaluation stated that, although there was no data to suggest that operator action could definitively have prevented the subsequent reactor scram, there were missed opportunities in the plant modification and preventive maintenance processes to evaluate current plant design and incorporate relevant mitigation strategies into operating procedures or follow-on plant modifications. Additionally, the evaluation reviewed the root cause investigation under AR 4509196 and determined that the review performed by the site at the time did not explore the ramifications of a similar failure mode in the valves open direction, resulting in another missed opportunity to mitigate this event.

Ultimately, the inspectors determined that the installation of the 2B FRV with a 14-inch stroke length introduced a latent design vulnerability into the system that went unidentified by the site until the event on November 4, 2022. Previous opportunities to identify the vulnerability through the licensees single point vulnerability assessments, as outlined in licensee procedure ER-AA-2004, "System and Component Vulnerability Identification and Mitigation,"

were unsuccessful because the licensee non-conservatively limited the scope of the vulnerability assessment to a narrow set of factors thought not to be applicable to the FRVs at the station due to the perceived robustness of the DFWLC system. When both internal and external operating experience revealed that the previous assumptions about the mitigating features of the DFWLC system were no longer valid, the site did not take meaningful action to reassess the risk of the system in accordance with AD-AA-3000 or revalidate the systems vulnerabilities in accordance with ER-AA-2004. As a result, the licensee did not have adequate station procedures or operations training to cope with the unique consequences of a failure of the 2B FRV as seen on November 4, 2022.

Corrective Actions: The licensee performed a root cause investigation of the event under AR 4534873. On November 6, 2022, the licensee established operation's department standing order 22-07 to provide specific guidance to operators regarding a repeat failure of the 2B FRV until permanent actions could be taken to eliminate the vulnerability. On January 21, 2023, the licensee installed a mechanical stop in the 2B FRV to physically limit its available stroke length and eliminate the design vulnerability noted above.

Corrective Action References: AR 4534873, "U2 Manual Scram on High Reactor Water Level"

Performance Assessment:

Performance Deficiency: The inspectors determined that the failure to have a procedure appropriate for the circumstance to address the unique plant vulnerability posed by a failure of the 2B feedwater regulation valve in the full open position was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Procedure Quality attribute of the Initiating Events cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations.

Significance: The inspectors assessed the significance of the finding using IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors screened the issue using IMC 0609, Appendix A, Exhibit 1, Initiating Events Screening Questions, and determined that this finding was of very low safety significance (Green).

Cross-Cutting Aspect: H.14 - Conservative Bias: Individuals use decision making-practices that emphasize prudent choices over those that are simply allowable. A proposed action is determined to be safe in order to proceed, rather than unsafe in order to stop. Specifically, the licensee failed to identify the latent design vulnerability of the 2B FRV through the licensees system and component vulnerability identification and mitigation program, as outlined in licensee procedure ER-AA-2004, because the scope of the vulnerability assessment was limited to a narrow set of factors thought not to be applicable to the FRVs at the station.

Enforcement:

Violation: Technical Specification 5.4.1, "Procedures," states that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. Regulatory Guide 1.33, "Quality Assurance Program Requirements," Appendix A, Section 6, lists procedures for combating emergencies and other significant events. Licensee procedure QCOA 0201-08, "Reactor High Water Level," and QCAN 901(2)-5 H-8, "1(2)B Feedwater Actuator Trouble,"

have been established by the licensee to combat a feedwater system failure under the purview of Regulatory Guide 1.33.

Contrary to the above, from approximately November 22, 1995, to November 6, 2022, neither licensee procedure QCOA 0201-08 or QCAN 901(2)-5 H-8 addressed the unique plant vulnerability posed by a failure of the 2B feedwater regulation valve in the full open position.

As a result, on November 4, 2022, following a failure of the 2B feedwater regulation valve to the full open position, operators were required to insert a manual trip of the reactor after reactor water level unexpectedly continued to rise following the automatic closure of the 2A feedwater regulation valve. The unexpected plant response was due to a latent design vulnerability which allowed the 2B feedwater regulation valve to be capable of passing greater than the required feedwater flow at full reactor power.

Enforcement Action: This violation is being treated as an NCV, consistent with Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On April 25, 2023, the inspectors presented the integrated inspection results to Brian Wake, Site Vice President, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection Type Designation Description or Title Revision or

Procedure Date

71111.01 Corrective Action AR 4666624 Tornado Warning Issued for QUAD CITIES STATION Area 03/31/2023

Documents

Procedures QCOA 0010-10 Tornado Watch/Warning, Severe Thunderstorm Warning, or 34

Severe High Winds

71111.04 Drawings M-39, Sheet 1 Diagram of Residual Heat Removal Piping 12/15/1997

M-39, Sheet 3 Diagram of Residual Heat Removal Piping 07/29/1999

Procedures QCOP 1300-01 RCIC System Preparation for Standby Operation 48

QOP 0020-03 Core Spray and RHR Room Draining 8

71111.05 Fire Plans FZ 11.1.3 Unit 1 RB 554'-0" Elev. HPCI & HPCI Access Tunnel 08/2022

FZ 8.2.7.A Unit 1 TB 615' Elev. Hydrogen Seal Oil Area and MCC's 09/2022

Procedures OP-AA-201-004 Fire Prevention for Hot Work 19

71111.06 Corrective Action AR 2604566 1-5799-2193 Check Valve Stuck Shut 12/25/2015

Documents AR 2604570 Small Water Leak Found in 901-33 Panel in Aux Elec. Room 12/25/2015

AR 306915 Water on Aux. Elect/Cable Spreading RM and Turb Bldg 03/01/2005

Floor

AR 4547214 1-5799-2203 Check Valve Sticking, Boiler Cond on Turb 01/08/2023

Deck

AR 4548199 Water Found in Aux Electric 01/12/2023

AR 4559676 Aux Electric Room Historic Leak Troubleshooting 03/06/2023

71111.12 Corrective Action AR 4523962 U2 EDG Failed to Start 09/22/2022

Documents

Miscellaneous DG6600-01 Maintenance Rule Systems Basis Document: Diesel 12/17/2014

Generator System

INPO Report Emergency Diesel Generator Failed to Start 09/22/2022

  1. 540170

NEI 18-10 Monitoring the Effectiveness of Nuclear Power Plant 07/2019

Maintenance

NUMARC 93-01 Industry Guideline for Monitoring the Effectiveness of 4A

Maintenance at Nuclear Power Plants

NDE Reports QDC-13774 Failure Analysis of Time Delay Relay 11/10/2022

Procedures ER-AA-2008 MSPI Failure Determination 4

ER-AA-320-1004 Maintenance Rule 18-10 - Performance Monitoring and 01

Inspection Type Designation Description or Title Revision or

Procedure Date

Dispositioning Between (a)(1) and (a)(2)

QCOS 6600-45 Unit 2 Diesel Generator Timed Start Test 29

Work Orders WO 5026561 EM EWP Perform 1/2 DG Time Delay Relay TD1,3,4 09/15/2021

Calibrations

71111.13 Procedures OU-AA-103 Shutdown Safety Management Program 23

OU-QC-104 Shutdown Safety Management Program Quad Cities Annex 24

QCOP 0600-02 Placing Main Feedwater Regulator Online or Offline 25

Work Orders WO 5146237 EMD U2 125 VDC Battery Charger #2 4HR Load Test 01/10/2023

WO 5308125 Unit 2 Scram on High Rx Water Lvl 11/07/2022

71111.15 Corrective Action AR 4505406 TIC 2-1141-14 Did Not Meet Acceptance Criteria

Documents AR 4508301 HPCI Pump Piping Connection Leaks 06/29/2022

AR 4542830 U2 HPCI Pump Piping Connection Leaks During Surveillance 12/14/2022

AR 4542921 Recommend Unit 2 SBLC Heat Trace Replacement

AR 4554301 Unexpected 901-8 A-4 Alarm 02/13/2023

AR 4558106 HPCI Signal Converter MGU Drive Signal (Auto) 02/25/2023

AR 4558498 Unit 1 HPCI Signal Converter Troubleshooting 03/01/2023

Drawings 4E-1649E Schematic and Wiring Diagram Window Display for 09/03/1998

Annunciator DG 1 and 2 Panel 2212-45

4E-2345, Sheet 1 Schematic Diagram 4160V Bus 23-1 Standby Diesel Half 03/17/1997

Feed Breakers

Engineering EC 365384 HPCI Turning Gear Performance on HPCI System 0

Changes Operability

EC 38025 ECR Pipe Freeze Seal Engineering Evaluation Request 0

EC 39729 Evaluation of Leakage at Mechanical Connections for Class 001

and 2 System Leakage Test at Quad Cities Unit 1 and Unit

EC 399498 HPCI Signal Converter Replacement 5

EC 4570013 Engineering Guidance on Performing Freeze Seal On-line 01/03/2023

EC 638226 Evaluate Min Wall Thickness for CREV Freeze Seal 0

Miscellaneous ASME BPVC XI ASME Boiler Pressure Vessel Code 2007

QC-S-2023-0008 50.59 Screening: QCOP and QCOS 2300 Series Procedure 03/02/2023

Changes to Leave the HPCI Turning Gear in PULL TO STOP

Procedures CC-AA-309-1011 General Piping Analysis 8

Inspection Type Designation Description or Title Revision or

Procedure Date

QCAN 2212-45 Overcurrent Trip of Diesel Generator to Bus 23-1 GCB 5

E-3

QCAN 901 (2)-5 Standby Liquid Control Tank High/Low Temperature 13

G-6

TIC 3697 Temporary Instruction Change to QCOS 2300-05: HPCI 91a

Pump Operability Test

Work Orders WO 05292138 (IST) (NEIL) HPCI Pump Operability 12/08/2022

WO 1956400-28 IM T/S FY 1-2386-B Servo Amp EC 399498 12/11/2022

71111.20 Engineering EC 404686 Decay Heat Removal Capability of RWCU System 0

Changes EC 623173 Alternate Decay Heat Removal (ADHR) System Qualification 0

for TS 3.4.8 Action A.1

Miscellaneous QDC-0200-M- Calculation of Reactor Drain Time in Support of DRAIN TIME 9

2339 Tool

Procedures QCAP 0260-03 Screening for Reactor Pressure Vessel Water Inventory 17

Control

71111.24 Corrective Action AR 4509198 Both Trains of SBGT Not Producing Required Flow 07/04/2022

Documents AR 4554207 1-1402-8B Failed to Reseat After 1400-01 02/13/2023

AR 4560494 Time Delay Relay 10-K45B As Found Out of Spec 03/08/2023

AR 4560646 Loose Wire Identified During Logic Test 03/09/2023

AR 4565295 PSU Q1R27 1-2301-4 LLRT Exceeded Admin Warning 15 03/27/2023

scfh

Drawings 4E-2765B Wiring Diagram Panel 902-47 06/10/2008

Engineering EC 399498 HPCI Signal Converter Replacement 5

Changes EC 637081 SBGT Surveillance Flowrate Note Below Expected Values 1

Procedures QCIS 1400-01 Core Spray Pump Discharge Pressure Calibration and 15

Functional Test

QCIS 1400-05 Core Spray Pump Discharge Flow Trip Unit Calibration and 10

Functional Test

QCOP 6600-12 Diesel Generator Air Start System Pressure Verification 13

QCOS 1000-28 RHR Service Water Pump Comprehensive/Performance Test 28

QCOS 1000-44 Unit 2 'B' Loop LPCI and Containment Cooling Modes of 31

HRHR Non-Outage Logic Test

QCOS 1300-05 RCIC Pump Operability Test 64

Inspection Type Designation Description or Title Revision or

Procedure Date

QCOS 1400-01 Core Spray System Flow Rate Test 52

QCOS 1400-01 Core Spray System Flow Rate Test 52

QCOS 1400-10 Core Spray Operability Verification 28

QCOS 2300-15 HPCI Drain Pot/Steam Line Drain Level Switch Valve, and 36

Alarm Functional Verification

QCOS 6500-09 Functional Test of Unit 1 Second Level Undervoltage 35

QCOS 6600-42 Unit 2 Emergency Diesel Generator Load Test 58

QCOS 6600-45 Unit 2 Diesel Generator Timed Start Test 29

QCOS 7500-05 SBGTS Operability Test 33

QCTS 2000-01 Drywell Leakage Troubleshooting 1

QOM 1-6500-T06 Bus 14-1 4160V AC K-D 4E-1304 8

TIC 3697 QCOS HPCI Pump Operability Test 1

2300-05

Self-Assessments RC 4509198 Root Cause: Both Trains of SBGT Not Producing Required 6

Flow

Work Orders QCOS 6600-41 U1 Emergency Diesel Generator Load Test 62

WO 5162728 'B' Loop LPCI RHR Cooling Modes Non-Outage Logic Test 03/08/2023

WO 5175095 'B' RHR Service Water Pump Comprehensive Test 01/17/2023

WO 5299623 Unit 2 EDG Starting Air Header PCV Reads High Out of 03/06/2023

Band

WO 5324924 Core Spray Pump a Flow Rate (IST) 03/22/2023

71152A Corrective Action AR 4511746 FRV Not Identified as SPV During ERVR4 07/19/2022

Documents AR 4534873 Unit 2 Scram on Rx High Water Level 11/04/2022

Miscellaneous NER NC-19-002- Feedwater Regulating Valve Fleetwide Issues 0

Y

NER NC-19-002- Feedwater Regulating Valve Fleetwide Issues 1

Y

QDC-0-2022- FRV Servo Valve 0

0153

QDC-0-2022- FRV Hydraulic Skid Particulate 0

0156

QDC-05-050 Station Design Inputs for EPU Margin Recovery Hydraulic 11/10/2005

Analysis

Inspection Type Designation Description or Title Revision or

Procedure Date

Standing Order 2B FRV Failure Results in U2 SCRAM 11/06/2022

2-07

Procedures ER-AA-2004 System & Component Vulnerability Identification and 12

Mitigation

18