05000265/LER-1994-001, Forwards LER 94-001-00.IST Procedures Revised to Incorporate Interim Procedure Requirements & RCIC Pump Tested Using Revised Procedures: Difference between revisions

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{{#Wiki_filter:__-                              _      .                  -.
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Commonwsalth Edison Quad Cities Nuclear Power Station O 22710 206 Avenue North Cordova, Illinois 61242 Telephone 309/654 2241 GGC-94-025 February 21. 1994 U.S. Nuclear Regulatory Commission Document Control Desk Washington. DC 20555
 
==Reference:==
Quad Cities Nuclear Power Station Docket Number 50-265. DPR-30. Unit Two                                ,
Enclosed is Licensee Event Report (LER) 94-001. Revision 00, for Quad Cities Nuclear Power Plant Station.
This report is submitted in accordance with the requirements of the Code of Federal Regulations, Title 10. Part 50.73(a)(2)(v)(D). The licensee shall report any event or condition that alone could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident.
The following commitments are being made by this letter:
Permanently revise the IST procedure to incorporate the interim procedure requirements.
Test the Unit 1 RCIC pump using the revised IST procedure in order to establish a new baseline. Since the next scheduled flowrate test for the Unit 1 RCIC is during the second quarter of 1994, and Unit I will be in a refuel outage, the Unit 1 RCIC will be tested upon unit.startup. Using the revised procedure will provide for meaningful trending of the pump degradation over the life of the pump, and will provide for appropriate corrective actions to be accomplished as a result of an adverse trend prior to exceeding the Technical Specification limits.
STMGRiO2594.GGC 9403040308 940221                                                y  ,          1 PDR    ADOCK 05000265                                                  l R                          PDR          ,
 
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If there are any questions or comments concerning this letter, please refer them to Nick Chrissotimos. Regulatory Performance Administrator at 309-654-2241, ext. 3100.
Respectfully, COMMONWEALTH EDISON COMPANY QUA9 CITIES NUCLEAR POWER STATION G. G. Campbell f
Station Manager GGC/TB/pim Enclosure cc:        J. Schrage T. Taylor INPO Records Center NRC Region III b
STMGRW2$94.GGC
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Latest revision as of 11:41, 6 September 2020

Forwards LER 94-001-00.IST Procedures Revised to Incorporate Interim Procedure Requirements & RCIC Pump Tested Using Revised Procedures
ML20067C871
Person / Time
Site: Quad Cities Constellation icon.png
Issue date: 02/21/1994
From: Campbell G
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
Shared Package
ML20067C873 List:
References
GGC-94-025, GGC-94-25, NUDOCS 9403040308
Download: ML20067C871 (2)


LER-2094-001, Forwards LER 94-001-00.IST Procedures Revised to Incorporate Interim Procedure Requirements & RCIC Pump Tested Using Revised Procedures
Event date:
Report date:
2652094001R00 - NRC Website

text

__- _ . -.

9 ,

Commonwsalth Edison Quad Cities Nuclear Power Station O 22710 206 Avenue North Cordova, Illinois 61242 Telephone 309/654 2241 GGC-94-025 February 21. 1994 U.S. Nuclear Regulatory Commission Document Control Desk Washington. DC 20555

Reference:

Quad Cities Nuclear Power Station Docket Number 50-265. DPR-30. Unit Two ,

Enclosed is Licensee Event Report (LER)94-001. Revision 00, for Quad Cities Nuclear Power Plant Station.

This report is submitted in accordance with the requirements of the Code of Federal Regulations, Title 10. Part 50.73(a)(2)(v)(D). The licensee shall report any event or condition that alone could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident.

The following commitments are being made by this letter:

Permanently revise the IST procedure to incorporate the interim procedure requirements.

Test the Unit 1 RCIC pump using the revised IST procedure in order to establish a new baseline. Since the next scheduled flowrate test for the Unit 1 RCIC is during the second quarter of 1994, and Unit I will be in a refuel outage, the Unit 1 RCIC will be tested upon unit.startup. Using the revised procedure will provide for meaningful trending of the pump degradation over the life of the pump, and will provide for appropriate corrective actions to be accomplished as a result of an adverse trend prior to exceeding the Technical Specification limits.

STMGRiO2594.GGC 9403040308 940221 y , 1 PDR ADOCK 05000265 l R PDR ,

.T ,

i i

If there are any questions or comments concerning this letter, please refer them to Nick Chrissotimos. Regulatory Performance Administrator at 309-654-2241, ext. 3100.

Respectfully, COMMONWEALTH EDISON COMPANY QUA9 CITIES NUCLEAR POWER STATION G. G. Campbell f

Station Manager GGC/TB/pim Enclosure cc: J. Schrage T. Taylor INPO Records Center NRC Region III b

STMGRW2$94.GGC

. b. .b

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