05000265/LER-1997-001, Forwards LER 97-001-00 Re Automatic Actuation of Any Esf. Commitments Made by Ltr,Listed

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Forwards LER 97-001-00 Re Automatic Actuation of Any Esf. Commitments Made by Ltr,Listed
ML20137H619
Person / Time
Site: Quad Cities Constellation icon.png
Issue date: 03/27/1997
From: Pearce L
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
Shared Package
ML20137H623 List:
References
LWP-97-029, LWP-97-29, NUDOCS 9704030001
Download: ML20137H619 (2)


LER-1997-001, Forwards LER 97-001-00 Re Automatic Actuation of Any Esf. Commitments Made by Ltr,Listed
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(v), Loss of Safety Function

10 CFR 50.73(a)(2)(iv), System Actuation
2651997001R00 - NRC Website

text

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Onnmoewcalth IMivm Company Quad 4.itics Generatmg St.ition 22710 2@th Asenue North Girdova, II. 612 42 C au Tei S m,u 22ii e

LWP-97-029 March 27, 1997 United States Nuclear Regulatory Commission Washington, DC 20555

. Attention:

Document Control Desk

Reference:

Quad Cities Nuclear Power Station Docket Number 50-265, DPR-30, Unit Two Enclosed is Licensee Event Report (LER)97-001, Revision 00, for Quad Cities Nuclear Power Station.

This report is submitted in accordance with the requirements of the Code of Federal Regulations, Title 10, Part 50.73(a)(2)(v)(D). The licensee shall report any event or condition that alone could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident.

t Also submitted in accordance with Part 50.73(a)(2)(iv).

The licensee l

shall report any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature.

The following commitments are being made by this letter:

1.

Communicate the specific management expectation for the person in charge of the work to review the appropriate prints to ensure that he/she is aware of the effects to plant and system operation from the activities performed.

(May 1, 1997).

2.

Communicate the specific management expectation that procedure writers include 10CFR50.59 safety screening / evaluation requirements in the associated procedure prerequisites.

(May 1, 1997).

3.

Revise QCAP 1100-04, " Procedure Revision, Review and Approval" to require the procedure prerequisites be bounded by the 10CFR50.59 safety screening / evaluation mode requirements.

Train all departments on this procedure change. (April 27, 1997).

4.

The Operations Manager and the Work Control Superintendent will meet with the Lead Unit Planners to provide expectations for i

Lead Unit Planner, Work Week Manager and Scheduler responsibilities when reviewing and scheduling work.

(April 30, 1997).

5.

Review and revise as necessary the work control procedures and

,0 m p licies t inc rp rate the expectations provided by the Operations Manager and Work Control Superintendent.

(June 1, 1997).

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I LWP-97-029 2

March 27, 1997 6.

Revise QCIPM 0100-10, " Refuel Outage ECCS Instrumentation Check Prior to ECCS Logic Test" to include prerequisites to identify the plant conditions required prior to using each section of j

this procedure and to clarify each of the individual impact statements.

(April 15, 1997).

7.

Instrument Maintenance shall review and establish a priority for-revising all of their power block procedures to determine if the impact statement or the prerequisite adequately identify the plant conditions that shall exist prior to. the use of the procedure.

(April 30, 1997).

If there are any questions or comments concerning this letter, please refer them to Charles Peterson, Regulatory Affairs Manager at 309-654-2241, ext. 3609.

Respectfully, COMMONWEALTH EDIS0N COMPANY QUAD CITIES NUCLEAR POWER STATION

$.0, b [

L. W. Pearce Station Manager LWP/CP/plm

. Enclosure cc:

A. B. Beach, Regional Administrator, Region III R.

M.. Pulsifer, Project Manager, NRR C. G. Miller, Senior Resident Inspector, Quad Cities W. D. Leech, MidAmerican' Energy Company D. C. Tubbs, MidAmerican Energy Company j

P. L. Piet, Licensing, Comed F. A. Spangenberg, Regulatory Affairs Manager, Dresden-INP0 Records Center I

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