04-27-2007 | On February 27, 2007 at 2300 hours0.0266 days <br />0.639 hours <br />0.0038 weeks <br />8.7515e-4 months <br />, control room operators commenced a power reduction on Unit 2 to 725 MWe to effect repairs on the 2C Reactor Feed Pump ( RFP) due to a seal leak. At approximately 2352 hours0.0272 days <br />0.653 hours <br />0.00389 weeks <br />8.94936e-4 months <br />, a pressure controller malfunction in the auxiliary steam supply to the 2A offgas train caused a reduction in its noncondensible gas removal efficiency. This malfunction impacted the 2A Offgas Preheater, Unit 2 steam dilution, and the 2A steam jet air ejector ( SJAE) operation, and caused increased condenser backpressure.
On February 28, 2007, at 0120 hours0.00139 days <br />0.0333 hours <br />1.984127e-4 weeks <br />4.566e-5 months <br />, Quad Cities Station Unit 2 Reactor was manually scrammed due to increasing condenser backpressure.
This event was caused by a blockage of the pressure sensing line to pressure controller (PC) 2-3041-3A with fine sized corrosion products. The increase in demand of PC 2-3041-3A caused relief valve (RV) 2-3099-129 to open, which ultimately caused a reduction in 2A SJAE efficiency and an increase in condenser backpressure.
The safety significance of this event was minimal. While this event required action to diagnose and initiate a manual scram, the reactor, turbine, condenser, and supporting systems performed as expected and within Technical Specifications and UFSAR limits. All safety systems remained fully functional during this event. |
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LER-2007-001, Manual Reactor Scram on Increasing Condenser Backpressure Due to a Decrease in 2A Offgas Train EfficiencyDocket Number |
Event date: |
02-28-2007 |
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Report date: |
04-27-2007 |
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Reporting criterion: |
10 CFR 50.73(a)(2)(iv)(A), System Actuation |
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2652007001R00 - NRC Website |
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FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6 PAGE (3) Quad Cities Nuclear Power Station Unit 2 05000265 NUMBER NUMBER (If more space is required, use additional copies of NRC Form 366A)(17)
PLANT AND SYSTEM IDENTIFICATION
General Electric - Boiling Water Reactor, 2957 Megawatts Thermal Rated Core Power Energy Industry Identification System (EIIS) codes are identified in the text as [XX].
EVENT IDENTIFICATION
Manual Reactor Scram on Increasing Condenser Backpressure Due to a Decrease in 2A Offgas Train Efficiency
A. CONDITION PRIOR TO EVENT
Event Time: 0120 hours0.00139 days <br />0.0333 hours <br />1.984127e-4 weeks <br />4.566e-5 months <br /> Reactor Mode: 1 Mode Name: Power OperationE Unit: 2 Event Date: February 28, 2007 Power Level: 30%
B. DESCRIPTION OF EVENT
On February 27, 2007, at 2300 hours0.0266 days <br />0.639 hours <br />0.0038 weeks <br />8.7515e-4 months <br />, control room operators commenced a power reduction on Unit 2 to 725 MWe to effect repairs on the 2C Reactor Feed [SJ] Pump [P] (RFP) due to a seal [SEAL] leak. At approximately 2352 hours0.0272 days <br />0.653 hours <br />0.00389 weeks <br />8.94936e-4 months <br />, condenser [SG] [COND] parameter trends began to change. The 2A Offgas [WF] Radiation Monitor [MON] indication began to decrease, condenser backpressure began to increase, and turbine [TA] exhaust hood temperatures began to increase. While the trend was visible in plant computerized trend data, the indications of this event were too small to be observed by control room operators monitoring their indications, annunciators, and alarms until February 28, 2007, at 0006 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> when the Unit 2 Operator identified condenser backpressure at 2.2 inches Hg and increasing.
Procedure QOA 3300-02, Loss of Condenser Vacuum, was entered. During the event briefing in the control room, operators dispatched personnel to check the offgas suction valve [ISV] position, refill the condenser loop seals, secure Offgas Air injection through the 2-2799-48 Air Flow Control Station Downstream Isolation valve, and started an emergency load drop on Unit 2. Condenser backpressure continued to increase. At 0120 hours0.00139 days <br />0.0333 hours <br />1.984127e-4 weeks <br />4.566e-5 months <br />, when condenser backpressure reached approximately 5 inches Hg, Unit 2 was manually scrammed in accordance with procedures.
At approximately 0700 hours0.0081 days <br />0.194 hours <br />0.00116 weeks <br />2.6635e-4 months <br />, walkdowns of steam-affected areas identified a steam leak from the Unit 2A Offgas Preheater Drain [DRN] Trap [TRP]. The Unit 2A Steam Jet Air Ejector (SJAE) [SH] supply pressure indication on PI 2-3041-4A was noted to be approximately 120 psig. The 2A offgas pressure control valve [PCV] normally controls auxiliary steam flow to the 2A SJAE at 127 psig.
At approximately 1140 hours0.0132 days <br />0.317 hours <br />0.00188 weeks <br />4.3377e-4 months <br />, the Offgas Trains were swapped from the 2A Train to the 2B Train. Dilution Steam pressure returned to 127 psig. This change occurred on the procedure step where auxiliary steam [SA] is isolated from the 2A Offgas Train.
Condenser backpressure and turbine hood temperatures recovered to within expected ranges. The Offgas Flow Recorder [FR] 2-5441-7 indicated an increase in flow rate for about two hours, then the flow values returned to within expected parameters for condenser in leakage.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6 PAGE (3) Quad Cities Nuclear Power Station Unit 2 05000265 NUMBER NUMBER (If more space is required, use additional copies of NRC Form 366A)(17) The steam leak from the 2A Offgas preheater drain trap was repaired. On April 9, 2007, the station reestablished the auxiliary steam to pressurize the 2A Offgas Train. When auxiliary steam was valved into the 2A Offgas Train, pressure controller [PC) PC 2-3041-3A did not sense auxiliary steam pressure, which then caused an increased steam flow to the 2A SJAE and increased pressurization of the auxiliary steam line. This caused the 2A SJAE relief valve [RV] RV 2-3099-129 to open. Troubleshooting identified the need to blow out foreign material in the sensing line for pressure controller PC 2-3041-3A. The accumulated debris was collected and identified as fine granular corrosion products, most likely from within the system.
On April 11, 2007, following repairs and calibration of the pressure control valve, the 2A Offgas Train was re-pressurized to verify corrective action effectiveness.
When the pressure control valve PCV 2-3099-29 was closed, the relief valve was observed again to be at 160 pounds pressure, which confirmed there was degradation of the pressure control valve. The pressure control valve was repaired on April 26, 2007.
C. CAUSE OF EVENT
Over time, internal corrosion products from the auxiliary steam piping system accumulated in the pressure sensing line for pressure controller PC 2-3041-3A. These corrosion products caused a blockage of the pressure sensing line to the controller, giving it a false increasing demand (Open) signal to the pressure control valve PCV 2-3099-29. This demand increased the pressure above the relief valve pressure setpoint, which caused relief valve RV 2-3099-129 to lift. The loss of auxiliary steam pressure from this sequence of events resulted in a reduction in 2A SJAE efficiency and ultimately an increase in the Unit 2 condenser backpressure.
There was apparent seat degradation of PCV 2-3099-29 when the valve was tested on April 11, 2007.B Based upon review of the events on February 28, 2007, this was considered collateral damage due to the effect of the blocked pressure sensing line and was not a direct contributor to the cause of the SJAE efficiency loss.
The steam leak downstream of the 2A offgas preheater, which was repaired on March 10, 2007, was a contributor to the reduction in dilution steam pressure margin, however, the leak was not large enough to be considered the root cause. A failure analysis on the piping and steam trap, along with fluid flow sensitivity studies and field testing, confirmed that the functionality of the 2A SJAE would not be lost by a leak of this size from the 2A SJAE. This leak was considered a contributing cause only because it marginally reduced the capacity of the Auxiliary Steam System to supply the 2A SJAE.
D.SSAFETY ANALYSIS The safety significance of this event was minimal. During this event, the highest condenser backpressure reached before the manual scram was 5.0 inches Hg. At this value, backpressure is below the setpoints for Reactor Scram (7.5 - 8.1 inches Hg), Turbine Trip (10 inches Hg), and Turbine Bypass Closure (23 inches Hg). While this event required action to diagnose and initiate a manual scram, the reactor, turbine, condenser, and supporting systems performed as expected and within Technical Specifications and UFSAR limits. During this event, all safety systems remained FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6 PAGE (3) Quad Cities Nuclear Power Station Unit 2 05000265 NUMBER NUMBER (If more space is required, use additional copies of NRC Form 366A)(17) fully functional, the scram was not complicated, and the normal heat sink was never lost.
This LER is being submitted in accordance with 10 CFR 50.73(a)(2)(iv)(A), which requires the reporting of any event or condition that resulted in manual or automatic actuation of the reactor protection system (RPS), including reactor scram or reactor trip.
E. CORRECTIVE ACTIONS
The steam leak on the 2A Offgas preheater drain trap was repaired.
Unit 2A SJAE sensing lines for auxiliary steam were blown down to remove any accumulated debris.
Units 1 and 2 SJAE sensing lines for auxiliary steam will be blown down periodically to remove any accumulated debris.
Unit 2A SJAE relief valve will be inspected or replaced.
Reviews of other Performance Centered Maintenance critical instruments on Main Steam, Feedwater Heaters, Gland Seal, Offgas, and Extraction Steam will be performed to determine if the loop calibration methodology for the preventive maintenance task requires a blowdown of the pressure sensing lines. Extent of Cause is limited to the methodology for calibrating pressure control valves in the auxiliary steam system that are subject to system internal corrosion product intrusion into the pressure sensing line.
F. PREVIOUS OCCURRENCES
No prior incidents involving a controller failure due to plugged sensing lines or a control valve failure due to plugged sensing lines were identified at Quad Cities over the past five years.
There were several instances of SJAE related issues over the past five years, however, they were not applicable to this event since they were focused on administrative issues, changes in dose rates, modification testing, or offgas noncondensible gas flow. None of these issues caused a loss of condenser vacuum due to SJAE efficiency losses from pressure control valve failures.
G. COMPONENT FAILURE DATA
The 2A SJAE pressure control valve (PCV 2-3099-29) is manufactured by Fisher Controls as Model Number 4160-657-DBQ. This is a 2.0 inch carbon steel M-Form valve with a 1500 psig rating, and a service rating for steam at 300-950 psig.
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05000498/LER-2007-001 | Turbine-Driven Auxiliary Feedwater Pump Failed to Start During Surveillance Testing (Supplement 1) | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000315/LER-2007-001 | -f Unit 1 Automatic Reactor Trip | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000263/LER-2007-001 | | | 05000266/LER-2007-001 | | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000269/LER-2007-001 | Dual Unit Trip from Jocassee Breaker Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000272/LER-2007-001 | ESF Actuation of Auxiliary Feedwater Pumps in Mode 3. | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000265/LER-2007-001 | Manual Reactor Scram on Increasing Condenser Backpressure Due to a Decrease in 2A Offgas Train Efficiency | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000278/LER-2007-001 | Laboratory Analysis Identifies Safety Relief Valves and Safety Valve Set Point Deficiencies | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000249/LER-2007-001 | Unit 3 High Pressure Coolant Injection System Declared Inoperable | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000282/LER-2007-001 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2007-001 | 450 Broadway, GSB P.O. Box 249 Buchanan, N.Y. 10511-0249Entergy Tel (914) 734-6700 Fred Dacimo Site Vice President Administration February 28, 2007 Indian Point Unit No. 2 Docket No. 50-247 NL-07-013 Document Control Desk U.S. Nuclear Regulatory Commission Mail Stop O-P1-17 Washington, DC 20555-0001 Subject:L Licensee Event Report # 2007-001-00, "Technical Specification Prohibited Condition Due to Exceeding the Allowed Completion Time for an Inoperable Residual Heat Removal Pump Due to an Electrical Supply Breaker Failure" Dear Sir: Pursuant to 10 CFR 50.73(a)(1), Entergy Nuclear Operations Inc. (ENO) hereby provides Licensee Event Report (LER) 2007-001-00. The enclosed LER identifies an event where the plant was operated in a condition prohibited by Technical Specifications, which is reportable under 10 CFR 50.73(a)(2)(i)(B). This condition has been recorded in the Entergy Corrective Action Program as Condition Report CR-IP2-2007-00013. There are no commitments contained in this letter. Should you or your staff have any questions regarding this matter, please contact Mr. Patric W. Conroy, Manager, Licensing, Indian Point Energy Center at (914) 734-6668. Sincerely, -Thr red R. Dacimo ite Vice President Indian Point Energy Center E Docket No. 50-247 NL-07-013 Page 2 of 2 Attachment: LER-2007-001-00 CC: Mr. Samuel J. Collins Regional Administrator — Region I U.S. Nuclear Regulatory Commission U.S. Nuclear Regulatory Commission Resident Inspector's Office Resident Inspector Indian Point Unit 2 Mr. Paul Eddy State of New York Public Service Commission INPO Record Center NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104DEXPIRES: 06/30/2007 (6-2004) Estimated burden per response to comply with this mandatory collection request: 50 hours.DReported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internetLICENSEE EVENT REPORT (LER) e-mail to infocollects@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-l0202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection. 2. DOCKET NUMBER 1 3. PAGE1. FACILITY NAME: INDIAN POINT 2 05000-247 1 OF 4 4. TITLE: Technical Specification Prohibited Condition Due to Exceeding the Allowed Completion Time for an Inoperable Residual Heat Removal Pump Due to an Electrical Supply Breaker Failure | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ix) | 05000483/LER-2007-001 | . Single Train Inoperability in the Essential Service Water System due to Inadequate Valve Closure Setup | | 05000286/LER-2007-001 | 450 Broadway, GSB P.O. Box 249 Buchanan, N.Y. 10511-0249Entergy Tel (914) 734-6700 Fred Dacimo Site Vice President June 4, 2007 Indian Point 3 Docket No. 50-286 N L-07-052 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Mail Stop O-P1-17 Washington, D.C. 20555-0001 Subject:LLicensee Event Report # 2007-001-00, "Manual Reactor Trip Due to Decreasing Steam Generator Levels as a Result of the Loss of Feedwater Flow Caused by the Failure of 32 Main Feedwater Pump Train A Control Logic Power Supply" Dear Sir or Madam: Pursuant to 10 CFR 50.73(a)(1), Entergy Nuclear Operations Inc. (ENO) hereby provides Licensee Event Report (LER) 2007-001-00. The attached LER identifies an event where the reactor was manually tripped while critical, which is reportable under 10 CFR 50.73(a)(2)(iv)(A) . This condition has been recorded in the Entergy Corrective Action Program as Condition Report CR-IP3-2007-01775. There are no new commitments identified in this letter. Should you have any questions regarding this submittal, please contact Mr. T. R. Jones, Manager, Licensing at (914) 734-6670. Sincerely, Fred R. Dacimo Site Vice President Indian Point Energy Center cc:LMr. Samuel J Collins, Regional Administrator, NRC Region I NRC Resident Inspector's Office, Indian Point 3 Mr. Paul Eddy, New York State Public Service Commission INPO Record Center pP,c.1)-1
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 EXPIRES: 6/30/2007 (6-2004) Estimated burden per response to comply with this mandatory collection request:D50 hours.DReportedDlessons learned areDincorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internetLICENSEE EVENT REPORT (LER) e-mail to infocollects@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection. 1. FACILITY NAME INDIAN POINT 3 2. DOCKET NUMBER 13. PAGE 05000-286 1 OFTD5 4. TITLE Manual Reactor Trip Due to Decreasing Steam Generator Levels as a Result of the Loss of Feedwater Flow Caused by the Failure of 32 Main Feedwater Pump Train A Control Logic Power Supply | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000293/LER-2007-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000306/LER-2007-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000309/LER-2007-001 | Uncompensated Degradation in a Security System | | 05000414/LER-2007-001 | Failure to Comply with Action Statement in Technical Specification (TS) 3.3.1 for Loss of a Channel of the Solid State Protection System | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000311/LER-2007-001 | Inoperability of the Chilled Water System - (21 and 22 Chillers Inoperable) | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000331/LER-2007-011 | . Undervoltage ConditiOn Resulted in the Actuation of the Emergency Diesel Generators | | 05000346/LER-2007-001 | Station Vent Radiation Monitor in Bypass due to Faulty Optical Isolation Board | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000348/LER-2007-001 | Vire President - Farley Operating Company, Inc. Po51 Office Drawer 470 Ashford, Alabarid 36312-0470 Tel 334 814 4511 Fax 334 814 4728 SOUTHERN June 22, 2007 COMPANY Energy to Serve Your World Docket Nos.: 50-348 NL-07-1231 50-364 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C. 20555-0001 Joseph M. Farley Nuclear Plant — Units 1 and 2
Licensee Event Report 2007-001-00
Technical Specification 3.8.1 Violation Due to
Failure of Breaker / Mechanism-Operated Cell Switch
Ladies and Gentlemen: Joseph M. Farley Nuclear Plant - Licensee Event Report (LER) No. 2007-001-00 is being submitted in accordance with 10 CFR 50.73(a)(2)(i)(B) and 10 CFR 50.73(a)(2)(v)(B). This letter contains no NRC commitments. If you have any questions, please advise. Sincerely, 7e. R. Johnson Vice President — Farley Joseph M. Farley Nuclear Plant 7388 North State Highway 95 Columbia AL 36319 JRJ/CHM Enclosure: Licensee Event Report 2007-001-00 - Unit 1 U. S. Nuclear regulatory Commission NL-07-1231 Page 2 cc:� Southern Nuclear Operating Company Mr. J. T. Gasser, Executive Vice President Mr. J. R. Johnson, Vice President — Farley Mr. D. H. Jones, Vice President — Engineering RTYPE: CFA04.054; LC # 14596 U. S. Nuclear Regulatory Commission Dr. W. D. Travers, Regional Administrator Ms. K. R. Cotton, NRR Project Manager — Farley Mr. E. L. Crowe, Senior Resident Inspector— Farley NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 06/30/2007 (6-2004) Estimated burden per response to comply with this mandatory collection request: 50 hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nudear Regulatory Commission, Washington, DC 2055570001, or by InternetLICENSEE EVENT REPORT (LER) e-mail to infocolledsanrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information(See reverse for required number of collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, thedigits/characters for each block) information collection. 1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE Joseph M. Farley Nuclear Plant - Unit 1 05000 348 1 OF 4 4. TITLE Technical Specification 3.8.1 Violation Due to Failure of Breaker / Mechanism-Operated Cell (MOC) Switch | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000316/LER-2007-001 | As-Found Local Leak Rate Tests Not Performed | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000456/LER-2007-001 | Unit 1 Reactor Trip Following a 345 Kv Transmission Line Lightning Strike | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000333/LER-2007-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000254/LER-2007-001 | Quad Cities Nuclear Power Station Unit 1 05000254 1 of 3 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000389/LER-2007-001 | S, Reactor Shutdown Due to Unidentified RCS Leakage | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000255/LER-2007-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000369/LER-2007-001 | 369 5McGuire Nuclear Station Unit 1 05000 1 OF5 | | 05000335/LER-2007-001 | Mispositioned Service Air Containment Isolation Valves | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000362/LER-2007-001 | Failure to declare Emergency Diesel Generator Inoperable and enter TS Action | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000353/LER-2007-001 | Scram Discharge Volume Vent and Drain Valves Opened Due To Fuse Removal | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000400/LER-2007-001 | Control Rod Shutdown Bank Anomaly Causes Entry into Technical Specification 3.0.3 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000261/LER-2007-001 | Reactor Trip Due to a Loose Wire in the Main Transformer Monitoring Circuitry | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000389/LER-2007-002 | 2B2 Reactor Coolant Pump (RCP) Seal Housing Leakage | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000255/LER-2007-002 | | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material | 05000395/LER-2007-002 | Failure to Follow Administrative Controls Results in LCO 3.6.4 Violation | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000306/LER-2007-002 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000440/LER-2007-002 | Shutdown Cooling Pump Trip Results in Operation Prohibited by Technical Specifications | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) | 05000414/LER-2007-002 | Technical Specification Violation Associated with Containment Valve Injection Water System | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000416/LER-2007-002 | Reactor SCRAM due to Turbine Trip caused by Loss of Condenser Vacuum | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv), System Actuation | 05000423/LER-2007-002 | Loss of Offsite Power Caused by Transmission System Operator While Defueled | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv), System Actuation | 05000311/LER-2007-002 | RReactor Trip Due to a Breach in the Condensate System | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000369/LER-2007-002 | | | 05000454/LER-2007-002 | Technical Specification Required Shutdown of Unit 1 and Unit 2 Due to an Ultimate Heat Sink Pipe Leak Common to Both Units | | 05000282/LER-2007-002 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | 05000315/LER-2007-002 | Failure to Declare Essential Service Water Inoperable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2007-002 | Technical Specification Prohibited Condition Due to Exceeding Containment Air Temperature Limit Allowed Outage Time as a Result of Changes in Instrument Uncertainty | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000250/LER-2007-002 | Completion of Shutdown Required by Technical Specifications due to Inoperable Rod Position Indication for Two Control Rods in the Same Control Bank | 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000353/LER-2007-002 | Automatic Actuation of Main Condenser Low Vacuum Isolation Logic During Refueling Outage | 10 CFR 50.73(a)(2)(iv), System Actuation | 05000272/LER-2007-002 | MManual Reactor Trips Due to Degraded Condenser Heat Removal | 10 CFR 50.73(a)(2)(iv)(A), System Actuation |
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