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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217D5211999-09-30030 September 1999 Informs That Remediating 3D Monicore Sys at Pbaps,Units 2 & 3 & 3D Monicore/Plant Monitoring Sys at Lgs,Unit 2 Has Been Completed Ahead of Schedule ML20216J3981999-09-29029 September 1999 Submits Comments for Lgs,Unit 1 & Pbaps,Units 2 & 3 Rvid,Rev 2,based on Review as Requested in GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20212J6561999-09-29029 September 1999 Informs of Completion of mid-cycle PPR of Limerick Generating Station on 990913.Identified No Areas in Which Licensee Performance Warranted Addl Insp Beyond Core Insp Program.Historical Listing of Plant Issues Encl ML20212H6401999-09-24024 September 1999 Forwards Revised Epips,Including Rev 11 to ERP-101 & Rev 18 to ERP-800.Copy of Computer Generated Rept Index Identifying Latest Revs of LGS Erps,Encl ML20212E7941999-09-22022 September 1999 Requests Authorization for Listed Licensed Operators to Temporarily Suspend Participation in Licensed Operator Requalification Program at LGS ML20212E8081999-09-22022 September 1999 Provides Notification That Listed Operators Have Been Permanently Reassigned to Duties That Do Not Require Maintaining Licensed Operator Status,Per 10CFR50.74 ML20212F5481999-09-20020 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing, for Pbaps,Units 2 & 3 & Lgs,Units 1 & 2 ML20212F8991999-09-17017 September 1999 Provides Written Confirmation That Thermo-Lag 330-1 Fire Barrier Corrective Actions at Lgs,Units 1 & 2 Have Been Completed 05000353/LER-1999-010, Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl1999-09-16016 September 1999 Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl ML20216F7821999-09-16016 September 1999 Forwards Insp Repts 50-352/99-05 & 50-353/99-05 on 990713-0816.One Violation Noted & Being Treated as NCV, Consistent with App C of Enforcement Policy.Violation Re Inoperability of Automatic Depression Sys During Maint ML20212A8751999-09-13013 September 1999 Forwards Safety Evaluation of First & Second 10-year Interval Inservice Insp Plan Request for Relief ML20211N5061999-09-0909 September 1999 Forwards TSs Bases Pages B 3/4 10-2 & B 3/4 2-4 for LGS, Units 1 & 2,being Issued to Assure Distribution of Revised Bases Pages to All Holders of TSs ML20212A0091999-09-0909 September 1999 Provides Notification That Licenses SOP-11172 & SOP-11321, for SO Muntzenberger & Rh Wright,Respectively,Are No Longer Necessary as Result of Permanent Reassignment ML20211P8571999-09-0808 September 1999 Forwards Reactor Operator Retake Exams 50-352/99-303OL & 50-353/99-303OL Conducted on 990812 ML20211P3891999-09-0303 September 1999 Informs That During 990902 Telcon Between J Williams & B Tracy,Arrangements Were Made for NRC to Inspect Licensed Operator Requalification Program at Plant.Insp Planned for Wk of 991018 05000352/LER-1999-009, Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed1999-09-0101 September 1999 Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed ML20211H2571999-08-26026 August 1999 Informs of Individual Exam Result on Initial Retake Exam on 990812.One Individual Was Administered Exam & Passed ML20211E9191999-08-24024 August 1999 Forwards fitness-for-duty Program Performance Data for Jan-June 1999 for PBAPS & LGS IAW 10CFR26.71(d).Data Includes Listed Info ML20211E9731999-08-23023 August 1999 Forwards LGS Unit 2 Summary Rept for 970228 to 990525 Periodic ISI Rept Number 5, Per TS SRs 4.0.5 & 10CFR50.55a(g) ML20211D6761999-08-20020 August 1999 Forwards non-proprietary Revised Emergency Response Procedures (Erps),Including Rev 29 to ERP-110, Emergency Notification & Rev 17 to ERP-800, Maint Team & Proprietary App ERP-110-1.App Withheld Per 10CFR2.790(a)(6) ML20210T4271999-08-13013 August 1999 Informs That NRC Revised Info in Rvid & Releasing Rvid Version 2 as Result of Review of 980830 Responses to GL 92-01 Rev 1,GL 92-01 Rev 1 Suppl 1 & Suppl Rai.Tacs MA1197 & MA1198 Closed ML20210U2211999-08-10010 August 1999 Forwards Insp Repts 50-352/99-04 & 50-353/99-04 on 990525-0712.One Violation Occurred & Being Treated as NCV, Consistent with App C of Enforcement Policy.Violation Re Late Performance of off-gas Grab Sample Surveillance 05000353/LER-1999-005, Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint1999-08-10010 August 1999 Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint ML20211B7881999-08-10010 August 1999 Transmits Summary of Two Meetings with Risk-Informed TS Task Force in Rockville,Md on 990514 & 0714 ML20210M7571999-08-0404 August 1999 Forwards Response to Requesting Addl Info Re Status of Decommissioning Funding for Lgs,Pbaps & Sngs. Attachment Provides Restatement of Questions Followed by Response ML20210P4191999-08-0404 August 1999 Forwards Initial Exam Repts 50-352/99-302 & 50-353/99-302 on 990702-04 (Administration) & 990715-22 (Grading).Six of Limited SRO Applicants Passed All Portion of Exam NUREG-1092, Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls1999-08-0303 August 1999 Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls ML20210L2011999-07-28028 July 1999 Forwards Final Personal Qualification Statement (NRC Form 398) for Reactor Operator License Candidate LB Mchugh ML20211F2641999-07-27027 July 1999 Forwards Three Copies of Rev 12 to LGS Physical Security Plan, Rev 4 to LGS Training & Qualification Plan & Rev 2 to LGS Safeguards Contingency Plan. Without Encls 05000352/LER-1999-008, Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator1999-07-23023 July 1999 Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator 05000353/LER-1999-004, Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs1999-07-23023 July 1999 Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs ML20210E6211999-07-22022 July 1999 Submits Rev to non-limiting Licensing Basis LOCA Peak Clad Temps (Pcts) for Limerick Generating Station (Lgs),Units 1 & 2 & Pbaps,Units 2 & 3 ML20216D3081999-07-19019 July 1999 Requests Renewal of OLs for Listed Individuals,Iaw 10CFR55.57.NRC Forms 398 & 396,encl for Applicants.Without Encl ML20216D8041999-07-19019 July 1999 Submits Summary of Final PECO Nuclear Actions Taken to Resolve Scram Solenoid Pilot Valve Issues Identified in Info Notice 96-007 05000352/LER-1999-006, Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error1999-07-12012 July 1999 Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error ML20209F6341999-07-0909 July 1999 Submits Supplemental Response to GL 94-03, Intergranular Stress Corrosion Cracking of Core Shrouds in Bwrs, for Unit 2.Rev 0 to 1H61R & GE-NE-B13-02010-33NP Repts & Revised Pages to Summary Rept Previously Submitted,Encl ML20209G9121999-07-0909 July 1999 Informs That Ja Hutton Has Been Appointed Director,Licensing for PECO Nuclear,Effective 990715.Previous Correspondence Addressed to Gd Edwards Should Now Be Sent to Ja Hutton ML20209C9041999-07-0808 July 1999 Forwards Monthly Operating Repts for June 1999 for Limerick Generating Station,Units 1 & 2 & Revised Monthly Repts for May 1999 ML20210B4441999-07-0808 July 1999 Forwards Preliminary NRC Form 398 & NRC Form 396 for Reactor Operator for License Candidate LB Mchugh.Candidate Failed Category B Portion of Operating Exam Given at LGS During Week of 990315.Tentative re-exam Has Been Scheduled 990812 05000353/LER-1999-003, Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure1999-07-0707 July 1999 Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure ML20209D8821999-07-0707 July 1999 Submits Estimate of Number of Licensing Actions Expected to Be Submitted in Years 2000 & 2001,as Requested by Administrative Ltr 99-02.Renewal Applications for PBAPS, Units 2 & 3,will Be Submitted in Second Half of 2001 ML20209D2671999-07-0202 July 1999 Responds to NRC 990322 & 0420 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20196J6301999-07-0101 July 1999 Requests Addl Info Re Status of Decommissioning Funding for Limerick Generating Station,Units 1 & 2,Peach Bottom Atomic Power Station,Units 1,2 & 3 & Salem Nuclear Generating Station,Units 1 & 2 05000352/LER-1999-004, Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys1999-07-0101 July 1999 Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys ML20209B7001999-06-30030 June 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20212J5401999-06-28028 June 1999 Discusses Completion of Licensing Action for NRC Bulletin 96-003, Potential Plugging of ECC Suction Strainers by Debris in Bwrs. Bulletin Closed for Unit 2 by NRC ML20207H8271999-06-24024 June 1999 Informs NRC That Util Has Completed Core Shroud Insps for LGS Unit 2.Proprietary Rept GE-NE-B13-02010-33P & non-proprietary Rev 0 to 1H61R,encl.Proprietary Rept Withheld,Per 10CFR2.790(a)(4) ML20196G7041999-06-24024 June 1999 Forwards Insp Repts 50-352/99-03 & 50-353/99-03 on 990413- 0524.No Violations Noted.Nrc Concluded That Licensee Staff Continued to Operate Both Units Safely ML20196A5641999-06-15015 June 1999 Provides Info Re Util Use of Four Previously Irradiated LGS, Unit 1,GE11 Assemblies in Unit 2 Cycle 6.Encl 990518 GE Ltr Provides Objective of Lead Use Assemblies Program & Outlines Kinds of Measurements That Will Be Made on Assemblies ML20195J6831999-06-11011 June 1999 Provides Proprietary Objectives for Lgs,Units 1 & 2,1999 Emergency Preparedness Exercise Scheduled to Be Conducted on 990914.Licensee Identifies Which Individuals Should Receive Copies of Info.Proprietary Info Withheld 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217D5211999-09-30030 September 1999 Informs That Remediating 3D Monicore Sys at Pbaps,Units 2 & 3 & 3D Monicore/Plant Monitoring Sys at Lgs,Unit 2 Has Been Completed Ahead of Schedule ML20216J3981999-09-29029 September 1999 Submits Comments for Lgs,Unit 1 & Pbaps,Units 2 & 3 Rvid,Rev 2,based on Review as Requested in GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20212H6401999-09-24024 September 1999 Forwards Revised Epips,Including Rev 11 to ERP-101 & Rev 18 to ERP-800.Copy of Computer Generated Rept Index Identifying Latest Revs of LGS Erps,Encl ML20212E7941999-09-22022 September 1999 Requests Authorization for Listed Licensed Operators to Temporarily Suspend Participation in Licensed Operator Requalification Program at LGS ML20212E8081999-09-22022 September 1999 Provides Notification That Listed Operators Have Been Permanently Reassigned to Duties That Do Not Require Maintaining Licensed Operator Status,Per 10CFR50.74 ML20212F5481999-09-20020 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing, for Pbaps,Units 2 & 3 & Lgs,Units 1 & 2 ML20212F8991999-09-17017 September 1999 Provides Written Confirmation That Thermo-Lag 330-1 Fire Barrier Corrective Actions at Lgs,Units 1 & 2 Have Been Completed 05000353/LER-1999-010, Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl1999-09-16016 September 1999 Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl ML20212A0091999-09-0909 September 1999 Provides Notification That Licenses SOP-11172 & SOP-11321, for SO Muntzenberger & Rh Wright,Respectively,Are No Longer Necessary as Result of Permanent Reassignment 05000352/LER-1999-009, Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed1999-09-0101 September 1999 Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed ML20211E9191999-08-24024 August 1999 Forwards fitness-for-duty Program Performance Data for Jan-June 1999 for PBAPS & LGS IAW 10CFR26.71(d).Data Includes Listed Info ML20211E9731999-08-23023 August 1999 Forwards LGS Unit 2 Summary Rept for 970228 to 990525 Periodic ISI Rept Number 5, Per TS SRs 4.0.5 & 10CFR50.55a(g) ML20211D6761999-08-20020 August 1999 Forwards non-proprietary Revised Emergency Response Procedures (Erps),Including Rev 29 to ERP-110, Emergency Notification & Rev 17 to ERP-800, Maint Team & Proprietary App ERP-110-1.App Withheld Per 10CFR2.790(a)(6) 05000353/LER-1999-005, Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint1999-08-10010 August 1999 Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint ML20210M7571999-08-0404 August 1999 Forwards Response to Requesting Addl Info Re Status of Decommissioning Funding for Lgs,Pbaps & Sngs. Attachment Provides Restatement of Questions Followed by Response ML20210L2011999-07-28028 July 1999 Forwards Final Personal Qualification Statement (NRC Form 398) for Reactor Operator License Candidate LB Mchugh ML20211F2641999-07-27027 July 1999 Forwards Three Copies of Rev 12 to LGS Physical Security Plan, Rev 4 to LGS Training & Qualification Plan & Rev 2 to LGS Safeguards Contingency Plan. Without Encls 05000352/LER-1999-008, Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator1999-07-23023 July 1999 Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator 05000353/LER-1999-004, Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs1999-07-23023 July 1999 Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs ML20210E6211999-07-22022 July 1999 Submits Rev to non-limiting Licensing Basis LOCA Peak Clad Temps (Pcts) for Limerick Generating Station (Lgs),Units 1 & 2 & Pbaps,Units 2 & 3 ML20216D3081999-07-19019 July 1999 Requests Renewal of OLs for Listed Individuals,Iaw 10CFR55.57.NRC Forms 398 & 396,encl for Applicants.Without Encl ML20216D8041999-07-19019 July 1999 Submits Summary of Final PECO Nuclear Actions Taken to Resolve Scram Solenoid Pilot Valve Issues Identified in Info Notice 96-007 05000352/LER-1999-006, Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error1999-07-12012 July 1999 Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error ML20209F6341999-07-0909 July 1999 Submits Supplemental Response to GL 94-03, Intergranular Stress Corrosion Cracking of Core Shrouds in Bwrs, for Unit 2.Rev 0 to 1H61R & GE-NE-B13-02010-33NP Repts & Revised Pages to Summary Rept Previously Submitted,Encl ML20209G9121999-07-0909 July 1999 Informs That Ja Hutton Has Been Appointed Director,Licensing for PECO Nuclear,Effective 990715.Previous Correspondence Addressed to Gd Edwards Should Now Be Sent to Ja Hutton ML20210B4441999-07-0808 July 1999 Forwards Preliminary NRC Form 398 & NRC Form 396 for Reactor Operator for License Candidate LB Mchugh.Candidate Failed Category B Portion of Operating Exam Given at LGS During Week of 990315.Tentative re-exam Has Been Scheduled 990812 ML20209C9041999-07-0808 July 1999 Forwards Monthly Operating Repts for June 1999 for Limerick Generating Station,Units 1 & 2 & Revised Monthly Repts for May 1999 05000353/LER-1999-003, Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure1999-07-0707 July 1999 Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure ML20209D8821999-07-0707 July 1999 Submits Estimate of Number of Licensing Actions Expected to Be Submitted in Years 2000 & 2001,as Requested by Administrative Ltr 99-02.Renewal Applications for PBAPS, Units 2 & 3,will Be Submitted in Second Half of 2001 ML20209D2671999-07-0202 July 1999 Responds to NRC 990322 & 0420 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves 05000352/LER-1999-004, Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys1999-07-0101 July 1999 Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys ML20209B7001999-06-30030 June 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20207H8271999-06-24024 June 1999 Informs NRC That Util Has Completed Core Shroud Insps for LGS Unit 2.Proprietary Rept GE-NE-B13-02010-33P & non-proprietary Rev 0 to 1H61R,encl.Proprietary Rept Withheld,Per 10CFR2.790(a)(4) ML20196A5641999-06-15015 June 1999 Provides Info Re Util Use of Four Previously Irradiated LGS, Unit 1,GE11 Assemblies in Unit 2 Cycle 6.Encl 990518 GE Ltr Provides Objective of Lead Use Assemblies Program & Outlines Kinds of Measurements That Will Be Made on Assemblies ML20195J6831999-06-11011 June 1999 Provides Proprietary Objectives for Lgs,Units 1 & 2,1999 Emergency Preparedness Exercise Scheduled to Be Conducted on 990914.Licensee Identifies Which Individuals Should Receive Copies of Info.Proprietary Info Withheld ML20195G4591999-06-10010 June 1999 Forwards MORs for May 1999 & Revised Repts for Apr 1999 for LGS Units 1 & 2 ML20195H0531999-06-0909 June 1999 Forwards Revised Bases Pages B3/4 10-2 & B3/4 2-4 for LGS Units 1 & 2,in Order to Clarify That Requirements for Reactor Enclosure Secondary Containment Apply to Extended Area Encompassing Both Reactor Enclosure & Refueling Area ML20195E7701999-06-0707 June 1999 Provides Notification of Change to NPDES Permit PA0052221, for Bradshaw Reservoir Facility Which Supports Operation of Lgs,Units 1 & 2,per EPP Section 3.2 ML20195C7631999-06-0101 June 1999 Notifies NRC That PECO Energy Has Completed Installation of New Large Capacity,Passive Strainers on RHR & Core Spray Sys Pump Suction Lines at Lgs,Unit 2,in Response to Ieb 96-003 ML20195D5381999-05-26026 May 1999 Forwards 1998 Occupational Exposure Tabulation Rept for LGS Units 1 & 2. Encl Is Diskette & Instructions.Rept Is Being re-submitted to Reset 12 Month Time Period.Without Disk ML20195B2821999-05-24024 May 1999 Requests That NRC Distribution Lists for LGS Be Updated. Marked-up Distribution List Showing Changes Is Attached ML20196L2891999-05-20020 May 1999 Provides Status Update of Thermo-Lag 330-1 Fire Barrier Corrective Actions,Iaw Commitments Made in ML20195B2951999-05-20020 May 1999 Forwards Rev 0 to LGS Unit 2 Reload 5,Cycle 6 COLR, IAW TS Section 6.9.1.12.Values Listed Have Been Determined Using NRC-approved Methodology & Are Established Such That All Applicable Limits of Plants Safety Analysis Are Met 05000352/LER-1999-003, Forwards LER 99-003-00,re Rps,Pcrvics Actuations.Ler Contains Special Rept Info for HPCI & Reactor Core Isolation Cooling Sys Injections Into Rv1999-05-19019 May 1999 Forwards LER 99-003-00,re Rps,Pcrvics Actuations.Ler Contains Special Rept Info for HPCI & Reactor Core Isolation Cooling Sys Injections Into Rv 05000353/LER-1999-002, Forwards LER 99-002-00,automatic Actuations of Primary Containment & Reactor Vessel Isolation Control Sys & Other Common Plant ESF Due to Loss of Power to a Rps/Ups Power Distribution Panel on 9904191999-05-18018 May 1999 Forwards LER 99-002-00,automatic Actuations of Primary Containment & Reactor Vessel Isolation Control Sys & Other Common Plant ESF Due to Loss of Power to a Rps/Ups Power Distribution Panel on 990419 ML20206E2001999-04-28028 April 1999 Forwards 1998 Annual Environ Operating Rept (Non- Radiological) for Limerick Generating Station,Units 1 & 2. Rept Submitted IAW Section 5.4.1 of App B of Fols,Epp (Non- Radiological) & Describes Implementation of EPP for 1998 ML20206D8801999-04-27027 April 1999 Forwards Rev 2 to LGS Unit 1 Reload 7,Cycle 8 COLR, IAW TS Section 6.9.1.12.COLR Provides cycle-specific Parameter Limits for Noted Info ML20206A5461999-04-21021 April 1999 Responds to Conference Call Between Util & NRC on 990420,re TS Change Request 98-07-2,revising TS Section 2.0 to Incorporate Revised MCPR Safety Limits.Attached Ltr Contains Info Requested ML20205T0441999-04-17017 April 1999 Forwards 1998 Annual Radiological Environ Operating Rept 15, IAW TS Section 6.9.1.7.REMP for 1998,confirmed That LGS Environ Effects from Radioactive Release Were Well Below LGS TSs & Other Applicable Regulatory Limits ML20205Q7581999-04-15015 April 1999 Forwards Response to RAI Re ISI Program First & Second 10-Yr Interval Relief Requests.Revs to Identified by Vertical Bar in Right Margin 1999-09-09
[Table view] Category:LEGAL/LAW FIRM TO NRC
MONTHYEARML20235T8911989-01-18018 January 1989 Forwards Endorsements 130 & 131 to Nelia Policy NF-164, Endorsements 107 & 108 to Maelu Policy MF-44,Endorsements 94 & 95 to Nelia Policy NF-107,Endorsements 110 & 111 to Nelia Policy NF-220 & Endorsements 97 & 98 to Maelu Policy MF-73 ML20196L5401988-07-0505 July 1988 Confirms 880705 Telcon Re Updated Antitrust Review for Facility.Nrc Agrees That Company Has Until 880815 to Respond to Request ML20235B2741987-02-19019 February 1987 FOIA Request for Documents Indicated on Encl Docket Sheets. Request Does Not Encompass Matl Already Available in PDR or Lpdr Denoted by Three or Four Asterisks on List ML20209G1461986-09-0909 September 1986 Requests Issuance of Subpoena for Rt Brown to Testify at Hearing Re Adequacy of Communications Sys Used to Mobilize Manpower Necessary to Evacuate State Correctional Institute in Graterford,Pa ML20214M6501986-09-0909 September 1986 Advises That Licensee Will Not Respond to Air & Water Pollution Patrol 860826 Response to Testimony Re Remand Hearing on Bus Drivers for Oj Roberts & Spring-Ford School Districts,Per Clements .Related Correspondence ML20214M6961986-09-0808 September 1986 Recommends Denial of Rl Anthony 860821 & 25 Petitions for Relief Per 10CFR50.100 & for Ofc of General Counsel Review of NRC 10CFR2.206 Decisions ML20205C4711986-08-0808 August 1986 Forwards 860808 Testimony of Vs Boyer & R Bradshaw Re Remand Hearing on Availability of Bus Drivers for Oj Roberts & Spring-Ford School Districts.Related Correspondence ML20212A7241986-07-24024 July 1986 Notifies That Testimony Presented at 860818 Hearing Will Reflect Revised Number of Volunteer Bus Drivers in Event School Evacuation Necessary ML20211Q1601986-07-21021 July 1986 Advises of Attempts to Deliver Volunteer Sheets of 570 Util Employees Agreeing to Drive Buses in Event of School Evacuation to Limerick Ecology Action (Lea) Headquarters. Related Correspondence ML20206P7421986-06-27027 June 1986 Forwards & Revised Proposed Stipulation in Response to PEMA Request for Changes to Stipulation Re Remanded Issue.Certificate of Svc Encl.Related Correspondence ML20206P9031986-06-26026 June 1986 Corrects Proposing Resolution of Remanded Issue Re Availability of School Bus Drivers for Oj Roberts & Spring-Ford School Districts.Correct Date of Stipulation Re Medical Svcs Is 860616 Instead of 851115 ML20206P7801986-06-25025 June 1986 Responds to AR Love,Counsel for Graterford Inmates,860618 Ltr Accusing Author of Providing ASLB Chairman H Hoyt W/ Trade Publications Re Emergency Planning Requirements. Attempt to Influence Chairman Denied ML20199E5131986-06-19019 June 1986 Forwards Affidavits of AL Bigelow & Vs Boyer Re Availability of Volunteer School Bus Drivers for Oj Roberts & Spring-Ford School Districts in Event of Evacuation,Per ML20199E6881986-06-18018 June 1986 Responds to Re Ex Parte Filing of Offsite Emergency Planning for Nuclear Power Plants:Case of Govt Gridlock. Ex Parte Filings by Rader Seen as Contributing to Lack of Impartiality.Related Correspondence ML20206D7631986-06-16016 June 1986 Forwards Licensee Proposal for Resolution of Remanded Issue Re Availability of School Bus Drivers for Oj Roberts & Spring-Ford School Districts,Per ASLB 860522 Order, Supporting Affidavits & Proposed Stipulation ML20211E7421986-06-11011 June 1986 Forwards Graterford Inmates Response to Aslab 860603 Order. W/O Encl.Related Correspondence ML20198E3721986-05-19019 May 1986 Advises That Excess Flow Check Valves,Described in Dec 1985 License Amend Application Can Be Tested During Plant Operation Using Addl Personnel & Special Procedures.Need for Amend Unaffected.Certificate of Svc Encl ML20197G7961986-05-13013 May 1986 Forwards,For Info,Delaware River Basin in Commission 860427 Revs 5 & 6 to Docket D-69-210 CP Re Dissolved Oxygen Limitations for Temp Constraints & Consumptive Use Allocations.Related Correspondence ML20203P9401986-05-0505 May 1986 Informs That Unit 1 Shut Down on 860502 for Approx 6 Wks During Which All Tests on Excess Flow Check Valves & Other Containment Isolation Valves Will Be Performed.Related Correspondence ML20203E4851986-03-12012 March 1986 FOIA Request for Effluent Rept 3 Submitted Under Encl Ltr. W/O Ltr ML20154L1531986-03-0606 March 1986 Forwards Appeal Board 850805 & Board 831115 Orders & Util to Nrc,Cited in 860219 Answer to Anthony late-filed Petition for Leave to Intervene,Per 860305 Request ML20140D9111986-01-28028 January 1986 Requests Denial of Rl Anthony 860117 Request for Suspension of License & Finding That Util Violated Conditions of License NPF-39 Due to Pending Application for Supplemental Cooling Water Supply ML20154B9491986-01-24024 January 1986 Forwards 851216 Application for Approval of Temporary Substitution of in-stream Monitoring of Dissolved Oxygen Levels in Place of 59 F Constraint on Withdrawals,Filed W/ State of DE River Basin Commission.Related Correspondence ML20138R4571985-12-24024 December 1985 Forwards Procedure M1-18, Decontamination & Treatment of Radioactively Contaminated Patient at Montgomery Hosp. Related Correspondence ML20138R4701985-12-24024 December 1985 Forwards Procedure M1-18, Decontamination & Treatment of Radioactively Contaminated Patient at Montgomery Hosp. Related Correspondence ML20137T2381985-12-16016 December 1985 Advises That 851213 Encl Figures May Be Illegible.Figures Taken Directly from Fsar.W/O Encl.Related Correspondence ML20137U1981985-12-0505 December 1985 Submits Correction to Transcript of Author 851204 Oral Argument on Fourth Partial Initial Decision.Substantive Changes on Pages 47 to 70 Should Be Made ML20136J1971985-11-20020 November 1985 Notifies That Author Will Appear to Present Oral Argument on 851204 on Behalf of Util Re Appeals of Fourth Partial Initial Decision,In Response to 851024 & 1106 Orders.Related Correspondence ML20133L7261985-10-22022 October 1985 Forwards Commonwealth of PA Court Decision Finding Bucks County & Neshaminy Water Resources Authority Obligated to Complete Point Pleasant Project.Related Correspondence ML20133J0491985-10-16016 October 1985 Lists Misspellings & Errors in Transcript of Author 851011 Oral Argument Before Aslab Re Third Partial Initial Decision ML20136C8271985-10-0404 October 1985 Forwards Delaware River Basin Commission 851002 Emergency Certification Granting Application for Use of Schuylkill River Whenever Flow at Pottstown Gage Over 415 Cubic Ft/ Second.Related Correspondence ML20133B0821985-09-30030 September 1985 Informs of Appearance to Present Oral Argument on 851011 Re Appeals of Third Partial Initial Decision in Proceeding,Per 850829 Order.Related Correspondence ML20136A8171985-09-23023 September 1985 Forwards Util Application W/Delaware River Basin Commission for Approval of Withdrawal of Water from Schuylkill River for Consumptive Use & Revised Application Permitting Release from Beachwood Pit.Related Correspondence ML20137Q4971985-09-18018 September 1985 Responds to Mi Lewis Request to Lift or Retract Cp.Petition for Relief Under Section 2.206 Should Be Denied.Puc of PA Recommended Decision Only Basis for Petition ML20137P9411985-09-17017 September 1985 Comments on ALAB-813,including Issuance of Final Findings Not Prerequisite to Authorizing Full Power OL & Error in Curtailing cross-exam Insufficient to Warrant Appellate Relief.Related Correspondence ML20137L4591985-09-0909 September 1985 Advises That Author,Atty for Graterford Inmates,Will Be Unavailable Until 851001.Related Correspondence ML20136A9731985-09-0404 September 1985 Forwards 850813 Notice of Commission Action Approving Application to Delaware River Basin Commission for Approval of Use of Consumptive Water Saved by Curtailment of Listed Plants,Per .Related Correspondence ML20133L8931985-08-0808 August 1985 Forwards Notice of Appeal Re Denial of Stay & Accompanying Memorandum of Law.W/O Encl.Related Correspondence ML20132E3341985-07-30030 July 1985 Informs That Applicant Will Not Respond to Air & Water Pollution Patrol Brief Until 30 Days After Svc of Appeal Brief to Be Filed by Graterford Inmates,Per 850725 Notice of Appeal,Unless Otherwise Directed by Appeal Board ML20126K7831985-07-26026 July 1985 Forwards Comments of Intervenor Graterford Prisoners,Per 850723 Order.W/O Encl.Related Correspondence ML20126L0031985-07-25025 July 1985 Forwards Graterford Inmates Notice of Appeal.W/O Encl. Related Correspondence ML20129C3171985-07-25025 July 1985 Advises That Delaware River Basin Commission Withholding Action on Addl Supplemental Water for Unit 1 Until NRC Authorizes Issuance of Full Power Ol.Requests Action on Full Power License as Soon as Possible ML20137S4861985-07-17017 July 1985 Forwards Util 850603 Application Under Section 3.8 of Delaware River Basin Compact for Use of Water from Beechwood Pit.Related Correspondence ML20128H1591985-07-0303 July 1985 Forwards Testimony of Jd Case.Related Correspondence ML20128F4121985-07-0303 July 1985 Advises of Return of Subpoena to Rl Morris Signed by ASLB on 850628.Morris Gave Deposition Voluntarily at Ofc on 850703 as Result of Arrangements Among Counsel Rather than at Time & Place Listed in Subpoena.Related Correspondence ML20128A2831985-06-28028 June 1985 Requests That ASLB Issue Subpoena Directing Rl Morris to Appear on 850702 in Philadelphia,Pa for Deposition.Rl Morris,Principal Witness Identified by Love on Contention Re Evacuation Time for Graterford.Related Correspondence ML20127L8131985-06-20020 June 1985 Forwards Revised Page 11 to Correct Typo in Applicant Renewed Motion for Exemption from 10CFR50.47(a) Requirements Per Two Contentions Admitted on Behalf of Graterford Prisoners During Litigation Period ML20126J8711985-06-10010 June 1985 Forwards Notice of Delaware River Basin Commission Action Re Temporary Mod to Increase Frequency of Water Withdrawn from Schuylkill River.Some Copies May Have Been Incorrectly Reproduced.Related Correspondence ML20126J7801985-06-0606 June 1985 Forwards 850603 Notice of Commission Action Re Temporary Mod of Delaware River Basin Decision for Facility,As Followup to .Related Correspondence ML20129A6121985-06-0303 June 1985 Forwards,For Info,Application Filed W/Delaware River Basin Commission for Approval for Use During 1985 of Consumptive Use Water Allocations of Titus Units 1,2 & 3 & Cromby Unit 2.Related Correspondence 1989-01-18
[Table view] |
Text
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LAW OFFICES CONNEn & WETTERII AIIN, P.C.
17 4 7 P EN N S Y LVA N I A AV E N U E. N. W.
Tnov m. cowwEn.dn. WASIflNOTON. D. C. 20000 MACK J. WETTENHANN NORENT M. MADEM DOUotAS X. OLSON
- Effx.'w"cH$5'"" April 12, 1985 NOBERT M. PUBL
- w. L CABLE ADDREM9; ATONLAW Mr. Harold R. Denton Director Office of Nuclear Reactor Regulation U.S. Nuclear Regulatory Commission
- Washington, D.C. 20555 In the Matter of Philadelphia Electric Company (Limerick Generating Station, Units 1 and 2)
Docket Nos. 50-352 and 50-353
Dear Mr. Denton:
By letter dated February 6, 1985, Philadelphia Electric Company responded to the petition submitted to you on December 23, 1984 by Robert L. Anthony for himself and on
' behalf of Friends of the Earth (collectively " FOE"). That petition requested relief pursuant to 10 C.F.R. S2.206 and was treated accordingly by the NRC. 50 Fed. Reg. 7152 (February 20, 1985).
In response, your letter to Mr. Anthony of February 13, 1985, stated that "[nlone of [the matters cited by FOE in its request] requires immediate action sought by the petition regarding continued operation of the facility."
FOE supplemented its request by letter dated February 25, 1985.
For the reasons stated in the attached comments of Philadelphia Electric Company, none of the other matters recently raised by FOE warrants the relief requested.
4 8504160418 850412 DR ADOCK 050 2 p$
I i
Mr. Harold R. Dsnton April 12, 1985 Page 2 Accordingly, . tthe petition for relief under Section 2.206 should be denied.
Sincerely, Mark J. Wetterhahn Counsel for the Licensee MJW/dlf Enclosure cc: Eugene J. Bradley, Esq.
L Robert L. Anthony
-M ___________ - . _ _ _ _ _ _ _ . _ _ _ . - - - _ - - . - - - - _ - _ - _ - - - - - - - _ -
l l
SUPPLEMENTAL COMMENTS OF PHILADELPHIA ELECTRIC COMPANY ON FOE'S LETTER DATED FEBRUARY 25, 1985 RELATING TO ITS REOUEST UNDER 10 C.F.R. S2.206 On February 6, 1985, Philadelphia Electric Company
("PECO") commented upon FOE's request under 10 C.F.R.
S2.206, pointing out that no basis in fact or law had been shown for' FOE's request that the NRC initiate proceedings to revoke the operating license for Unit 1 of the Limerick Generating Station (" Limerick") by issuing an order to show cause. In its letter dated February 25, 1985, FOE sets forth additional matters in support of its request for relief. As discussed below, the specific items set forth by FOE demonstrate a misunderstanding of the facts as well as the importance of the matters it seeks to raise.
The documents cited by FOE were generated by PECO and the NRC in their ongoing inspections and safety reviews and therefore do not constitute any new information. Moreover the items raised by FOE do not pose any threat to the public health and safety.
The various documents cited by FOE include a Systematic Assessment of Licensee Performance ("SALP") Report, NRC
. inspection reports, PECO's Licensee Event Reports ("LER's")
M and related correspondence.1/ In adjudicatory proceedings,
,the boards have rejected similar claims presented on the basis of such information already in the record. Before addressing the specific matters raised by FOE, PECO there-
~ fore will review some of'those decisions.
Adjudicatory Decisions Allegations like FOE's have typically been raised in licensing proceedings in the context of quality assurance issues. The Boards have ruled that the mere recitation of isolated deficiencies and violations does not raise any litigable issue and has no particular safety significance to the plant.
For example, in Callaway, the Appeal Board stated:
In any project even remotely ap-proaching in magnitude and complexity the erection of a nuclear power plant, there inevitably will be some con-struction defects tied to quality assurance lapses.- It would therefore be totally unreasonable to hinge the grant of an NRC operating license upon a demonstration of error-free con-struction. Nor is such a result mandat-ed by either the Atomic Energy Act of 1954, as amended, or the Commission's implementing regulations. What they require is simply a finding of reason-able assurance that, as built, the facility can and will be operated L without endangering the public health i.
and safety. . . . Thus, in examining i
l 1/ Inasmuch as all of the matters raised by FOE pertain to documents in- the record, we assume that the Commission's Statement of Policy on handling late allegations is inapplicable. See 50 Fed. Reg. 11030 (March 19, 1985).
L i
~
- claims of quality assurance defi- !
ciencies, one must look to the implica-tion of those deficiencies in terms of safe plant operation.2/
Reiterating this standard in Shoreham, the Appeal Board rejected intervenor's argument that "every deficiency, however minor, reflects an attitude or lack of discipline that undermines confidence that the QA program has been successful."3/ The Board agreed that deficiencies or violations lack safety significance where found "to be rinor, readily correctable, and posing no concern about the adequacy of [ plant] design, construction or installation."AI The Licensing Board in Shoreham disapproved an inter-venor's use of the same approach taken by FOE in its Section 2.206 petition, which it characterized as " bean counting."
It stated:
This Board is not about to become involved in a " numbers game" of counting beans of different colors in viewing the examples of OA failures relied on by
[ petitioner]. Rather, we- have kept foremost in our minds the intent of the NRC requirements and the actual and practical measures taken to meet these requirements to assure no undue risk to the health and safety of the public. We seek a solid foundation for finding reasonable assurance of adequate pro-tection of the health and safety of the
-2/ Union Electric Company (Callaway Plant, Unit 1) ,
ALAB-740, 18 NRC 343, 346 (1983).
3/ Long Island Lighting Company (Shoreham Nuclear Power Station, Unit 1), ALAB-788, 20 NRC 1102, 1141 (1984).
4/ Id. at 1142.
7
_4_
public. -We do not seek evidence of a sterile application of ritualistic methodology.5/
As the Licensing Board in Perry similarly stated:
The test of a QA program, however, lies not only in its ability to uncover discrepancies in QA but also in its ability to cope with them successfully so that they are remedied and that assurance of safe construction can ultimately be found.6/
In issuing its Partial Initial Decision on a quality assur-ance contention, the Board in Perry rejected far more sweeping claims than those alleged by FOE and held:
The construction of Perry is a massive task. We are not surprised that applicant's quality assurance program has detected thousands of nonconfor-mances that have arisen during con-struction. . . . There is no indication that there are serious problems that have escaped detection or are not being carefully tracked and resolved.7/
Regarding the matter of corrective actions for noncon-formance reports identified in notices of violation and SALP's, the Board in Perry further stated:
5/ Shoreham, supra, LBP-83-57, 18 NRC 445, 579-60 (1983),
aff'd, ALAB-788, 20 NRC 1102 (1984). The Board noted that the NRC Staff "has looked at many different ways of counting violations, and has found such ' bean' counting to be essentially meaningless." M. at 604-05.
6/ Cleveland Electric Illuminating Company (Perry Nuclear Power Plant, Units 1 and 2) , LBP-83-74, 18 NRC 1241, 1252 (1983).
7/ Perry, supra, LBP-83-77, 18 NRC 1365, 1367-68 (1983).
~
T The intervenors have not raised any serious doubts about the adequacy of the closeout systems. The. Board is entirely satisfied that applicant's system is closely tracking the status of NRs at Perry, and that nonconformances are being properly closed out in a manner consistent with their safety signifi-cance.
. . . These matters must be examined in context. We would be concerned if it appeared that applicant was not ade-quately monitoring the safety signifi-cance and status of ARs [ audit action reports]; however, the record indicates otherwise. Applicant's procedural system, and its use of this system to correct problems, in our view reflect a proper degree of involvement and con-trol. Intervenors have not indicated any evidence that casts doubt on this conclusion.8_/
Overall, the Board in Perry found that violations and deficiencies discussed in NRC investigative reports and SALP's " disclosed no serious inadequacies" and were general-ly " associated with the first phase of a major new work activity, where ' start-up' deficiencies may be more likely."
The Board concluded that, considering the breadth of the Staff's investigation and inspections, there was not a
" disproportionate number of noncompliances," which "were of a relatively low severity level."EI 8_/ M . at 1387, 1389.
9/ Id. at 1393-94.
7
.Other boards have similarly found that minor violations and deficiencies-do.not raise any substantial issues regard-ing the public health and safety. In Comanche Peak, the Licensing Board rejected a late contention . relating to deficiencies'in the applicant's hot functional testing where the petitioner simply recited,' "without any analytical differentiation or sense of priority, dozens of specific
. omissions and problems." b -The Board stated:
We.do not find these omissions or the discovery. of problems to have been startling or disturbing. The staff states that the plant cannot load fuel until staff is satisfied that it is safe
'to 'go to power.. The staff must be
. satisfied that it' is safe to. load fuel even though. certain items have not received hot- functional testing. It also must be sure that each of the
-problem areas:has been resolved.
. . . [The proposed contention] contains a very detailed description of omissions of- equipment during hot -functional testing, but 'it does not give a basis for believing that any of those omissions has safety significance.
Similarly, it points out problems found by applicant during its own test, but it does not provide any basis for believing that. the discovery of these problems indicates some safety deficiency in the construction of the plant.11/
.10f 0 Texas Utilities Generating Com?any (Comanche Peak Steam
-Electric Station, Units 1 anc. 2) , LBP-83-75A, 18 NRC
.1260,-1262 (1983).
-11/ Id. at 1262-63. As the Board added: " Individual
. problems found in the course of a testing program only
. indicate that the program is working. Unless there is (Footnote Continued)
I
_7_
f In the Byron proceeding, the Licensing Board rejected ~
requests to reopen the record based upon NRC inspection 4
reports on preoperational testing, which noted minor noncom-( pliances equivalent to those cited by FOE in its petition.
The Board held that "the events reportnd in the inspection reports did not seem to rise to [the) level" of indicating any institutional incapacity in applicant's quality assur-ance program.N Notably, the Staff testified in an affida-vit opposing reopening that Severity Level IV violations are not a significant safety issue and that, due to the complex-ity and scope of the preoperational testing program at a nuclear power plant, including the large number of inspector hours, "the identification of many items of noncompliance is not unexpected."EI During the hearing in Byron, the Staff reiterated its testimony that a higher number of deficiencies would be expected during inspection of preoperational testing activ-ities, and that the safety significance of noncompliances must be analyzed "in the context of the SALP evaluations and other controlling factors . . . such as the civil penalties, (Footnote Continued) additional basis, discovered problems are not in themselves grounds for admitting a contention." I_d. d at 1264 n.6.
p/ Commonwealth Edison Company (Byron Nuclear Power Station, Units 1 and 2) , LBP-83-41, 18 NRC 104, 110 (1983).
13/ Id. at 107.
the severity levels of the noncompliances, the amount of activity at a particular site', the phase of the activity (e.g., construction approaching fuel loading), the number of inspector-hours, the age of the plant, and the utility's response to.the citations." N!
The Director of the Office of Inspection and Enforce-ment denied relief under Section 2.206 in Point Beach where the petitioner, like FOE, argued that Severity Level IV and V violations warranted the relief. After examining the SALP reports for Point Beach "to determine whether they illus-trate a decline in performance that is significant enough to j require issuance of an order to show cause why the license should not be modified, suspended, or revoked," the Staff i
" concluded that they do not" inasmuch as the overall perfor-mance of the licensee "was never considered unsatisfac-tory."EI As in Point Beach, the Staff should also conclude in this instance that the Severity Level IV and V violations-cited by petitioner, which "had limited safety signifi-cance," do not justify " escalated enforcement action" such as issuance of an order to show cause.E!
M/ Byron, supra, LBP-84-2, 19 NRC 36, 119 (1984).
M/ Wisconsin Electric Power Company (Point Beach Nuclear Plant, Units 1 and 2) , DD-83-13, 18 NRC 721, 722-23 (1983).
16/ Id. at 722..
3 Matters Alleged By FOE With'the approach of the adjudicatory boards and Staff in other proceedings as background, we now address the various categories of items raised by FOE. The first matter raised by FOE is an NRC SALP Report for Limerick dated January 14, 1985. FOE cites construction deficiency reports filed from December 1, 1983 through November 30, 1984 as listed in Table 1 of the SALP Report. The reporting of such deficiencies, however, is merely evidence that PECO's quality assurance program is working and does not indicate any hazard to the public health and safety in the operation of Limerick. Similarly, the mere recitation of Severity Level IV and V violations in Table 3, in a project of the magnitude of Limerick, does not indicate any problem in meeting regulatory standards or any hazard to the public health and safety.
The particular items upon which FOE has focused do not demonstrate any basis for instituting license revocation proceedings. As with any SALP Report, areas in which the-NRC has found a need for improvement are discussed. The summary of the SALP Report, nevertheless, expressly states that "the quality of construction activities remained high" -
during the assessment period and that "[m]anagement involve-ment was evident." ! The SALP Report further states that M/ SALP Report at 6 (January 14, 1985),
7 the " level of-performance of preoperational testing activ-ities improved over that shown in the previous assessment" and that "lfcensee management took adequate corrective actions to address [previously identified] weaknesses after they were identified by the NRC."E Further, the NRC found in the SALP Report that the contribution to the overall quality of the program made by the licensee's Test Review Board . to be " noteworthy," and
" amply demonstrated during NRC's programmatic reviews."N!
In conclusion, the NRC determined that the " level of perfor-mance attained by the end . of the preoperational phase appears to have carried over into the startup pha se . " 2 0
Accordingly, the NRC rated PECO's performance in con-struction activities as Category I, consistent trend.E 18/ Id.
19/ Id.
20/ Id. In the more detailed discussion of construction Etivities, .the SALP Report states: "The licensee maintained good performance throughout this assessment period. Significant amounts of NRC inspection effort bore out the conclusion that the quality of construction was maintained at a high level." Id. at 9.
21/ Id. at 11. A SALP Report designation of Category 1 means: " Reduced NRC attention may be appropriate.
Licensee management attention and involvement are aggressive and oriented toward nuclear safety; licensee resources are ample and ef fectively used such that a high level of performance with respect to operational safety or construction is being achieved." M. at 4.
L_.
i T
_ 11 Thereafter, FOE cites a number of NRC inspection
. reports and PECO LER's , whose results were incorporated within the SALP-Report. FOE's discussion of these reports
.is wholly lacking in a.ny analysis of demonstrated or poten-tial safety significance. No basis exists to support the sweeping allegation that each of the events reported by PECO "had_ the potential to precipitate a nuclear accident."E!
For example, the most recent report cited by FOE, Inspection Report No. 50-352/85-08 (February 1, 1985), contains a single Severity Level IV violation. Page four of the Report describes the short-term and long-term corrective actions proposed by the licensee to enhance operator familiarity
-with Technical Specification requirements and procedural guidance to operators. FOE also cites inspection reports not analyzed in the February 14, 1985 SALP Report. None of those reports, however, cites violations more serious than a Severity Level IV.E!
FOE asserts that it has "no indication that there was any summary or review of open inspection items, exceptions, M/ Letter dated February 25, 1985 from Robert L. Anthony to Harold R. Denton, Director, NRC Of fice. of ' Nuclear Reactor Regulation (" FOE letter of February 25, 1985")
at 1.
-23/
See FOE letter dated February 25, 1985 at 3. Moreover, FOE has apparently misinterpreted certain reports, i.e., treating the discussion of open items in Inspection Report 50-352/84-72 and 50-352/84-66 as involving new items.
violations or deviations which were-required to be resolved" prior to criticality for Unit 1.EI No reference is made to any specific item listed in the license.E Inasmuch as the NRC need not accord " presumptive validity"- to FOE's conjecture that certain requirements might not have been met, it is unnecessary for the NRC to institute a proceeding to establish affirmatively that those conditions have been met. Obviously, this is a matter of ongoing staff review and will necessarily be examined in the issuance of a full-power license.EI 24/ Id.
-25/ See License No. NPF-27 (Attachment 1, Item 4) (October 26, 1984).
M/ Northern Indiana Public Service Company (Bailly Generating Station, Nuclear-1), CLI-78-7, 7 NRC 429,
'432 (1978). The Bailly standard was recently reiterated by the Licensing Board in Kerr-McGee
' Chemical Corporation (Kress Creek Decontamination),
Docket No. 40-2061-SC, "Second Prehearing Conference Memorandum and Order" (February 7, 1985) (slip op. at
- 7) .
E/ See 10 C.F.R. 550.57 (a) . As the Appeal Board stated in Summer, it is the Staff which is obligated "to insure the existence of an adequate basis for each of the requisite Section 50.57 determinations" before the issuance of the operating license. South Carolina Electric & Gas Company (Virgil C. Summer Nuclear Station, Unit 1), ALAB-642, 13 NRC 881, 896 (1981).
Subsequently in that case, the Licensing Board denied a motion to reopen on the ground that it "could do no more than order that (alleged deficiencies] be corrected and that the corrections be monitored by Staff - a procedure that is already in effect without Board intervention." Summer, supra, " Memorandum and Order" (April 28, 1982) (slip op. at 4).
13 -
In effect, FOE has disregarded the presumption that the Staff will perform its statutory and regulatory . functions properly.EI As the Commission found in the WPPSS proceed-ing: "Past practice clearly indicates that . . . the agency has ' faithfully discharged' its responsibility to give full consideration to petitions seeking relief under section 2.206."E!
The next portion of FOE's supplemental request asserts I
the " inevitability" of an accident at Limerick due to the number of LER's from October 26, 1984 through January 31, 1985. A few particular LER's are briefly described, but there is no discussion of the significance of the reported event in terms of any specific relief alleged to be appro-
.priate under Section 2.206. Contrary to FOE's implicit assertion, the Director has never held that the mere filing of an LER or a number of LER's provides a basis for relief under Section 2.206. The Commission's statements of consid-eration in adopting 10 C.F.R. S50.73 make it clear that an LER does not necessarily involve an incident of such safety significance as to justify the extraordinary relief sought
-28/ E.g., Consumers Power Company (Midland Plant, Units 1 and 2) , Docket Nos. 50-329-OL and 50-330-OL, "Special Prehearing Conference Order" (February 23, 1979) (slip op. at 2).
2_9_/ Washington Public Power Supply System (WPPSS Nuclear Project - Nos. 1 & 2) , CLI-82-29, 16 NRC 1221, 1229 (1982).
7
~
_ 14 _
by FOE.E!
As the Board noted in Shearon Harris, the number of LER's depends greatly upon the age of the plant, the utility's relationship with the NRC Office of Inspection and Enforcement, and the licensee's attitude in reporting reportable occurrences. The Staff testified that a high number of LER's may be "due to the licensee's determination to report all possible reportable items," and the Board agreed that a licensee's reporting policy "may be an overriding factor" where a high number of LER's are report-ed . 3_1,/ The Board further noted, significantly, that "a 30/ Thus, the Commission stated that "the LER will be a detailed narrative description of potentially significant safety events," which "will provide the basis for the careful study of events or conditions that might lead to serious accidents." 48 Fed. Reg.
33850, 33853 (July 26, 1983) (emphasis added). The Commission added: "If the NRC staff decides that the event was especially significant from the standpoint of safety, the staff may request that the licensee provide additional information and data associated with the event." M. The Commission specifically stated that the LER rule requires that events be reported "regardless of the safety significance of the components, systems, or structures involved." I_d . The Board in Perry granted summary disposition on a contention based on LER's because it was " unwilling to assume without more specific argument that issuance of LER's, which are expected to be generated from a quality assurance program, represent a breakdown in that program." Cleveland Electric Illuminating Company (Perry Nuclear Power Plant, Units 1 & 2), LBP-82-ll4, 16 NRC 1909, 1917 (1982).
31/ Carolina Power and Light Company (Shearon Harris Nuclear Power Plant, Units 1, 2, 3 and 4) , LBP-79-19, 10 NRC 37, 72 n.16 (1979).
higher-number of LER's naturally occur at the startup of a l
plant."E! l In any event, PECO has responded to the concerns expressed by the NRC regarding the number of LER's. As stated in recent correspondence to the NRC, the corrective action programs previously discussed with the NRC have been effective in reducing the number of reportable events.3_3/
As noted in that correspondence, corrective action programs have been implemented to eliminate recurring design defi-ciencies, address personnel errors and make programmatic improvements. As further stated, positive results have been demonstrated.
FOE's assertions regarding the completion of surveil-lance tests required under License No. NPF-27 are very unclear. Contrary to its assertion that certain surveil-lance tests must be completed prior to initial criticality to meet the conditions in License No. NPF-27, Attachment 1, l
32/ Id. at 72.
3 3_3/ See Letter dated April 2, 1985 from M.J. Cooney,.
Manager, Nuclear Production, Electric Production i
Department, to Richard W. Starostecki, Director, Division of Projects and Resident Programs, Region I, NRC. As a threshold matter, the number of LER's reported by PECO is substantially attributable to conservative reporting techniques and actuation of emergency safeguard features, which merely provides confirmation that the systems perform as designed. M.
I at 4. No event resulted in serious degradation of safety barriers or the ability to achieve or maintain safe shutdown. Id. at 5.
I L
O those provisions of the license deal with preoperational tests and other items, not surveillance tests. In any event, Inspection Report No. 84-71 states in Paragraph 3.4 at page 5:- "The inspector reviewed the surveillance tests listed in Appendix B to verify they were conducted prior to entering Operational Condition 2." This led to the follow-ing finding at page 6:
The pre initial criticality activities were adequately accomplished. The surveillance tests reviewed were accom-plished prior to entering Operational Condition 2. The licensee management was carefully monitoring those activ-ities necessary to enter Operational Condition 2 and was observed to perform overview checks of alarm / annunciator status on at least two occasions.
The last items cited by FOE as a basis for its request are taken from the Independent Design Review of Limerick Generating Station, Unit No. 1, Core Spray System (November 1984) ("IDR"), prepared by Torrey Pines Technology. FOE states that it is not " persuaded" by the explanation at page 29 of the report which addresses ten items for which docu-ments required by the General Electric design control program to demonstrate a design adequacy review were not
, available. No technical basis is cited by FOE for its disagreement with the conclusion by Torrey Pines that it is
1 satisfied with the resolution of the unavailable documenta-tion. b FOE also cites IDR findings which " identified several errors and inconsistencies in the analysis that was used to show plant safe shutdown capability following postulated breaks in the core spray line."EI FOE overlooks the fact, however, that Torrey Pines also found that the corrective action adopted by PECO " adequately addresses the concerns raised by the Finding."E! This involves a thorough review and revision of "all safety evaluation calculations associ-ated with jet impingement," including analysis of loss of individual devices with an individual worst single failure 34/ Specifically, Torrey Pines concluded that "GE's actions in response to the (finding], when successfully implemented, will adequately address all concerns which led to the Finding classification." Torrey Pines found that GE's re-creation of the design review and document release process "provided a high degree of assurance that all required reviews were performed and documented," and also noted that "GE will be performing a technical review of the 10 items identified with missing design review documents." All of this, concluded Torrey Pines, "will provide the action necessary to assure that no safety problem would be created as a result of missing design review documents." Torrey Pines IDR, Vol. 2, at 29.
3_5) Those errors related to the availability of certain safety systems when transmitters were lost as a result of jet impingement. The IDR concluded that determining the impact of those errors "would have required a knowledge of all plant systems and components that
'could not be gained in this TPT review of the core spray system." Torrey Pines IDR, Vol. 2, at 56.
36/ Id. at 57.
1 and loss of.all devices from a common cause with the worst common single _ failure.EI The NRC Staff performed an inspection on January-15, 1985 to verify implementation of this corrective action plan and determined the corrective actions to be acceptable.EI Contrary to FOE's implication, the Torrey Pines IDR did not find that its analysis of postulated breaks in the core spray lines imputed problems to "all plant systems and components."EI Rather, Torrey Pines concluded that it could not evaluate the impact of errors it found without performing analyses based upon a knowledge of "all plant systems and components." This simply means that such analyses were beyond the scope of Torrey Pine's charter in preparing the IDR.
In conclusion, FOE has alleged nothing which would warrant the initiation of a proceeding pursuant to 10 C.F.R.
S2.206 to revoke the operating license for Limerick, Unit 1.
Accordingly, the relief requested by FOE should be denied.
37/ Id. at 56-57.
M/ Summary of Meeting on Independent Design Verification Program Held January 10, 1985 (February 20, 1985).
-39/ Id. at 56. See FOE letter dated February 25, 1985 at E