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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217D5211999-09-30030 September 1999 Informs That Remediating 3D Monicore Sys at Pbaps,Units 2 & 3 & 3D Monicore/Plant Monitoring Sys at Lgs,Unit 2 Has Been Completed Ahead of Schedule ML20216J3981999-09-29029 September 1999 Submits Comments for Lgs,Unit 1 & Pbaps,Units 2 & 3 Rvid,Rev 2,based on Review as Requested in GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20212J6561999-09-29029 September 1999 Informs of Completion of mid-cycle PPR of Limerick Generating Station on 990913.Identified No Areas in Which Licensee Performance Warranted Addl Insp Beyond Core Insp Program.Historical Listing of Plant Issues Encl ML20212H6401999-09-24024 September 1999 Forwards Revised Epips,Including Rev 11 to ERP-101 & Rev 18 to ERP-800.Copy of Computer Generated Rept Index Identifying Latest Revs of LGS Erps,Encl ML20212E7941999-09-22022 September 1999 Requests Authorization for Listed Licensed Operators to Temporarily Suspend Participation in Licensed Operator Requalification Program at LGS ML20212E8081999-09-22022 September 1999 Provides Notification That Listed Operators Have Been Permanently Reassigned to Duties That Do Not Require Maintaining Licensed Operator Status,Per 10CFR50.74 ML20212F5481999-09-20020 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing, for Pbaps,Units 2 & 3 & Lgs,Units 1 & 2 ML20212F8991999-09-17017 September 1999 Provides Written Confirmation That Thermo-Lag 330-1 Fire Barrier Corrective Actions at Lgs,Units 1 & 2 Have Been Completed 05000353/LER-1999-010, Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl1999-09-16016 September 1999 Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl ML20216F7821999-09-16016 September 1999 Forwards Insp Repts 50-352/99-05 & 50-353/99-05 on 990713-0816.One Violation Noted & Being Treated as NCV, Consistent with App C of Enforcement Policy.Violation Re Inoperability of Automatic Depression Sys During Maint ML20212A8751999-09-13013 September 1999 Forwards Safety Evaluation of First & Second 10-year Interval Inservice Insp Plan Request for Relief ML20211N5061999-09-0909 September 1999 Forwards TSs Bases Pages B 3/4 10-2 & B 3/4 2-4 for LGS, Units 1 & 2,being Issued to Assure Distribution of Revised Bases Pages to All Holders of TSs ML20212A0091999-09-0909 September 1999 Provides Notification That Licenses SOP-11172 & SOP-11321, for SO Muntzenberger & Rh Wright,Respectively,Are No Longer Necessary as Result of Permanent Reassignment ML20211P8571999-09-0808 September 1999 Forwards Reactor Operator Retake Exams 50-352/99-303OL & 50-353/99-303OL Conducted on 990812 ML20211P3891999-09-0303 September 1999 Informs That During 990902 Telcon Between J Williams & B Tracy,Arrangements Were Made for NRC to Inspect Licensed Operator Requalification Program at Plant.Insp Planned for Wk of 991018 05000352/LER-1999-009, Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed1999-09-0101 September 1999 Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed ML20211H2571999-08-26026 August 1999 Informs of Individual Exam Result on Initial Retake Exam on 990812.One Individual Was Administered Exam & Passed ML20211E9191999-08-24024 August 1999 Forwards fitness-for-duty Program Performance Data for Jan-June 1999 for PBAPS & LGS IAW 10CFR26.71(d).Data Includes Listed Info ML20211E9731999-08-23023 August 1999 Forwards LGS Unit 2 Summary Rept for 970228 to 990525 Periodic ISI Rept Number 5, Per TS SRs 4.0.5 & 10CFR50.55a(g) ML20211D6761999-08-20020 August 1999 Forwards non-proprietary Revised Emergency Response Procedures (Erps),Including Rev 29 to ERP-110, Emergency Notification & Rev 17 to ERP-800, Maint Team & Proprietary App ERP-110-1.App Withheld Per 10CFR2.790(a)(6) ML20210T4271999-08-13013 August 1999 Informs That NRC Revised Info in Rvid & Releasing Rvid Version 2 as Result of Review of 980830 Responses to GL 92-01 Rev 1,GL 92-01 Rev 1 Suppl 1 & Suppl Rai.Tacs MA1197 & MA1198 Closed ML20210U2211999-08-10010 August 1999 Forwards Insp Repts 50-352/99-04 & 50-353/99-04 on 990525-0712.One Violation Occurred & Being Treated as NCV, Consistent with App C of Enforcement Policy.Violation Re Late Performance of off-gas Grab Sample Surveillance 05000353/LER-1999-005, Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint1999-08-10010 August 1999 Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint ML20211B7881999-08-10010 August 1999 Transmits Summary of Two Meetings with Risk-Informed TS Task Force in Rockville,Md on 990514 & 0714 ML20210M7571999-08-0404 August 1999 Forwards Response to Requesting Addl Info Re Status of Decommissioning Funding for Lgs,Pbaps & Sngs. Attachment Provides Restatement of Questions Followed by Response ML20210P4191999-08-0404 August 1999 Forwards Initial Exam Repts 50-352/99-302 & 50-353/99-302 on 990702-04 (Administration) & 990715-22 (Grading).Six of Limited SRO Applicants Passed All Portion of Exam NUREG-1092, Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls1999-08-0303 August 1999 Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls ML20210L2011999-07-28028 July 1999 Forwards Final Personal Qualification Statement (NRC Form 398) for Reactor Operator License Candidate LB Mchugh ML20211F2641999-07-27027 July 1999 Forwards Three Copies of Rev 12 to LGS Physical Security Plan, Rev 4 to LGS Training & Qualification Plan & Rev 2 to LGS Safeguards Contingency Plan. Without Encls 05000352/LER-1999-008, Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator1999-07-23023 July 1999 Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator 05000353/LER-1999-004, Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs1999-07-23023 July 1999 Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs ML20210E6211999-07-22022 July 1999 Submits Rev to non-limiting Licensing Basis LOCA Peak Clad Temps (Pcts) for Limerick Generating Station (Lgs),Units 1 & 2 & Pbaps,Units 2 & 3 ML20216D3081999-07-19019 July 1999 Requests Renewal of OLs for Listed Individuals,Iaw 10CFR55.57.NRC Forms 398 & 396,encl for Applicants.Without Encl ML20216D8041999-07-19019 July 1999 Submits Summary of Final PECO Nuclear Actions Taken to Resolve Scram Solenoid Pilot Valve Issues Identified in Info Notice 96-007 05000352/LER-1999-006, Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error1999-07-12012 July 1999 Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error ML20209F6341999-07-0909 July 1999 Submits Supplemental Response to GL 94-03, Intergranular Stress Corrosion Cracking of Core Shrouds in Bwrs, for Unit 2.Rev 0 to 1H61R & GE-NE-B13-02010-33NP Repts & Revised Pages to Summary Rept Previously Submitted,Encl ML20209G9121999-07-0909 July 1999 Informs That Ja Hutton Has Been Appointed Director,Licensing for PECO Nuclear,Effective 990715.Previous Correspondence Addressed to Gd Edwards Should Now Be Sent to Ja Hutton ML20209C9041999-07-0808 July 1999 Forwards Monthly Operating Repts for June 1999 for Limerick Generating Station,Units 1 & 2 & Revised Monthly Repts for May 1999 ML20210B4441999-07-0808 July 1999 Forwards Preliminary NRC Form 398 & NRC Form 396 for Reactor Operator for License Candidate LB Mchugh.Candidate Failed Category B Portion of Operating Exam Given at LGS During Week of 990315.Tentative re-exam Has Been Scheduled 990812 05000353/LER-1999-003, Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure1999-07-0707 July 1999 Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure ML20209D8821999-07-0707 July 1999 Submits Estimate of Number of Licensing Actions Expected to Be Submitted in Years 2000 & 2001,as Requested by Administrative Ltr 99-02.Renewal Applications for PBAPS, Units 2 & 3,will Be Submitted in Second Half of 2001 ML20209D2671999-07-0202 July 1999 Responds to NRC 990322 & 0420 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20196J6301999-07-0101 July 1999 Requests Addl Info Re Status of Decommissioning Funding for Limerick Generating Station,Units 1 & 2,Peach Bottom Atomic Power Station,Units 1,2 & 3 & Salem Nuclear Generating Station,Units 1 & 2 05000352/LER-1999-004, Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys1999-07-0101 July 1999 Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys ML20209B7001999-06-30030 June 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20212J5401999-06-28028 June 1999 Discusses Completion of Licensing Action for NRC Bulletin 96-003, Potential Plugging of ECC Suction Strainers by Debris in Bwrs. Bulletin Closed for Unit 2 by NRC ML20207H8271999-06-24024 June 1999 Informs NRC That Util Has Completed Core Shroud Insps for LGS Unit 2.Proprietary Rept GE-NE-B13-02010-33P & non-proprietary Rev 0 to 1H61R,encl.Proprietary Rept Withheld,Per 10CFR2.790(a)(4) ML20196G7041999-06-24024 June 1999 Forwards Insp Repts 50-352/99-03 & 50-353/99-03 on 990413- 0524.No Violations Noted.Nrc Concluded That Licensee Staff Continued to Operate Both Units Safely ML20196A5641999-06-15015 June 1999 Provides Info Re Util Use of Four Previously Irradiated LGS, Unit 1,GE11 Assemblies in Unit 2 Cycle 6.Encl 990518 GE Ltr Provides Objective of Lead Use Assemblies Program & Outlines Kinds of Measurements That Will Be Made on Assemblies ML20195J6831999-06-11011 June 1999 Provides Proprietary Objectives for Lgs,Units 1 & 2,1999 Emergency Preparedness Exercise Scheduled to Be Conducted on 990914.Licensee Identifies Which Individuals Should Receive Copies of Info.Proprietary Info Withheld 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217D5211999-09-30030 September 1999 Informs That Remediating 3D Monicore Sys at Pbaps,Units 2 & 3 & 3D Monicore/Plant Monitoring Sys at Lgs,Unit 2 Has Been Completed Ahead of Schedule ML20216J3981999-09-29029 September 1999 Submits Comments for Lgs,Unit 1 & Pbaps,Units 2 & 3 Rvid,Rev 2,based on Review as Requested in GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20212H6401999-09-24024 September 1999 Forwards Revised Epips,Including Rev 11 to ERP-101 & Rev 18 to ERP-800.Copy of Computer Generated Rept Index Identifying Latest Revs of LGS Erps,Encl ML20212E7941999-09-22022 September 1999 Requests Authorization for Listed Licensed Operators to Temporarily Suspend Participation in Licensed Operator Requalification Program at LGS ML20212E8081999-09-22022 September 1999 Provides Notification That Listed Operators Have Been Permanently Reassigned to Duties That Do Not Require Maintaining Licensed Operator Status,Per 10CFR50.74 ML20212F5481999-09-20020 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing, for Pbaps,Units 2 & 3 & Lgs,Units 1 & 2 ML20212F8991999-09-17017 September 1999 Provides Written Confirmation That Thermo-Lag 330-1 Fire Barrier Corrective Actions at Lgs,Units 1 & 2 Have Been Completed 05000353/LER-1999-010, Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl1999-09-16016 September 1999 Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl ML20212A0091999-09-0909 September 1999 Provides Notification That Licenses SOP-11172 & SOP-11321, for SO Muntzenberger & Rh Wright,Respectively,Are No Longer Necessary as Result of Permanent Reassignment 05000352/LER-1999-009, Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed1999-09-0101 September 1999 Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed ML20211E9191999-08-24024 August 1999 Forwards fitness-for-duty Program Performance Data for Jan-June 1999 for PBAPS & LGS IAW 10CFR26.71(d).Data Includes Listed Info ML20211E9731999-08-23023 August 1999 Forwards LGS Unit 2 Summary Rept for 970228 to 990525 Periodic ISI Rept Number 5, Per TS SRs 4.0.5 & 10CFR50.55a(g) ML20211D6761999-08-20020 August 1999 Forwards non-proprietary Revised Emergency Response Procedures (Erps),Including Rev 29 to ERP-110, Emergency Notification & Rev 17 to ERP-800, Maint Team & Proprietary App ERP-110-1.App Withheld Per 10CFR2.790(a)(6) 05000353/LER-1999-005, Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint1999-08-10010 August 1999 Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint ML20210M7571999-08-0404 August 1999 Forwards Response to Requesting Addl Info Re Status of Decommissioning Funding for Lgs,Pbaps & Sngs. Attachment Provides Restatement of Questions Followed by Response ML20210L2011999-07-28028 July 1999 Forwards Final Personal Qualification Statement (NRC Form 398) for Reactor Operator License Candidate LB Mchugh ML20211F2641999-07-27027 July 1999 Forwards Three Copies of Rev 12 to LGS Physical Security Plan, Rev 4 to LGS Training & Qualification Plan & Rev 2 to LGS Safeguards Contingency Plan. Without Encls 05000352/LER-1999-008, Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator1999-07-23023 July 1999 Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator 05000353/LER-1999-004, Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs1999-07-23023 July 1999 Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs ML20210E6211999-07-22022 July 1999 Submits Rev to non-limiting Licensing Basis LOCA Peak Clad Temps (Pcts) for Limerick Generating Station (Lgs),Units 1 & 2 & Pbaps,Units 2 & 3 ML20216D3081999-07-19019 July 1999 Requests Renewal of OLs for Listed Individuals,Iaw 10CFR55.57.NRC Forms 398 & 396,encl for Applicants.Without Encl ML20216D8041999-07-19019 July 1999 Submits Summary of Final PECO Nuclear Actions Taken to Resolve Scram Solenoid Pilot Valve Issues Identified in Info Notice 96-007 05000352/LER-1999-006, Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error1999-07-12012 July 1999 Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error ML20209F6341999-07-0909 July 1999 Submits Supplemental Response to GL 94-03, Intergranular Stress Corrosion Cracking of Core Shrouds in Bwrs, for Unit 2.Rev 0 to 1H61R & GE-NE-B13-02010-33NP Repts & Revised Pages to Summary Rept Previously Submitted,Encl ML20209G9121999-07-0909 July 1999 Informs That Ja Hutton Has Been Appointed Director,Licensing for PECO Nuclear,Effective 990715.Previous Correspondence Addressed to Gd Edwards Should Now Be Sent to Ja Hutton ML20210B4441999-07-0808 July 1999 Forwards Preliminary NRC Form 398 & NRC Form 396 for Reactor Operator for License Candidate LB Mchugh.Candidate Failed Category B Portion of Operating Exam Given at LGS During Week of 990315.Tentative re-exam Has Been Scheduled 990812 ML20209C9041999-07-0808 July 1999 Forwards Monthly Operating Repts for June 1999 for Limerick Generating Station,Units 1 & 2 & Revised Monthly Repts for May 1999 05000353/LER-1999-003, Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure1999-07-0707 July 1999 Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure ML20209D8821999-07-0707 July 1999 Submits Estimate of Number of Licensing Actions Expected to Be Submitted in Years 2000 & 2001,as Requested by Administrative Ltr 99-02.Renewal Applications for PBAPS, Units 2 & 3,will Be Submitted in Second Half of 2001 ML20209D2671999-07-0202 July 1999 Responds to NRC 990322 & 0420 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves 05000352/LER-1999-004, Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys1999-07-0101 July 1999 Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys ML20209B7001999-06-30030 June 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20207H8271999-06-24024 June 1999 Informs NRC That Util Has Completed Core Shroud Insps for LGS Unit 2.Proprietary Rept GE-NE-B13-02010-33P & non-proprietary Rev 0 to 1H61R,encl.Proprietary Rept Withheld,Per 10CFR2.790(a)(4) ML20196A5641999-06-15015 June 1999 Provides Info Re Util Use of Four Previously Irradiated LGS, Unit 1,GE11 Assemblies in Unit 2 Cycle 6.Encl 990518 GE Ltr Provides Objective of Lead Use Assemblies Program & Outlines Kinds of Measurements That Will Be Made on Assemblies ML20195J6831999-06-11011 June 1999 Provides Proprietary Objectives for Lgs,Units 1 & 2,1999 Emergency Preparedness Exercise Scheduled to Be Conducted on 990914.Licensee Identifies Which Individuals Should Receive Copies of Info.Proprietary Info Withheld ML20195G4591999-06-10010 June 1999 Forwards MORs for May 1999 & Revised Repts for Apr 1999 for LGS Units 1 & 2 ML20195H0531999-06-0909 June 1999 Forwards Revised Bases Pages B3/4 10-2 & B3/4 2-4 for LGS Units 1 & 2,in Order to Clarify That Requirements for Reactor Enclosure Secondary Containment Apply to Extended Area Encompassing Both Reactor Enclosure & Refueling Area ML20195E7701999-06-0707 June 1999 Provides Notification of Change to NPDES Permit PA0052221, for Bradshaw Reservoir Facility Which Supports Operation of Lgs,Units 1 & 2,per EPP Section 3.2 ML20195C7631999-06-0101 June 1999 Notifies NRC That PECO Energy Has Completed Installation of New Large Capacity,Passive Strainers on RHR & Core Spray Sys Pump Suction Lines at Lgs,Unit 2,in Response to Ieb 96-003 ML20195D5381999-05-26026 May 1999 Forwards 1998 Occupational Exposure Tabulation Rept for LGS Units 1 & 2. Encl Is Diskette & Instructions.Rept Is Being re-submitted to Reset 12 Month Time Period.Without Disk ML20195B2821999-05-24024 May 1999 Requests That NRC Distribution Lists for LGS Be Updated. Marked-up Distribution List Showing Changes Is Attached ML20196L2891999-05-20020 May 1999 Provides Status Update of Thermo-Lag 330-1 Fire Barrier Corrective Actions,Iaw Commitments Made in ML20195B2951999-05-20020 May 1999 Forwards Rev 0 to LGS Unit 2 Reload 5,Cycle 6 COLR, IAW TS Section 6.9.1.12.Values Listed Have Been Determined Using NRC-approved Methodology & Are Established Such That All Applicable Limits of Plants Safety Analysis Are Met 05000352/LER-1999-003, Forwards LER 99-003-00,re Rps,Pcrvics Actuations.Ler Contains Special Rept Info for HPCI & Reactor Core Isolation Cooling Sys Injections Into Rv1999-05-19019 May 1999 Forwards LER 99-003-00,re Rps,Pcrvics Actuations.Ler Contains Special Rept Info for HPCI & Reactor Core Isolation Cooling Sys Injections Into Rv 05000353/LER-1999-002, Forwards LER 99-002-00,automatic Actuations of Primary Containment & Reactor Vessel Isolation Control Sys & Other Common Plant ESF Due to Loss of Power to a Rps/Ups Power Distribution Panel on 9904191999-05-18018 May 1999 Forwards LER 99-002-00,automatic Actuations of Primary Containment & Reactor Vessel Isolation Control Sys & Other Common Plant ESF Due to Loss of Power to a Rps/Ups Power Distribution Panel on 990419 ML20206E2001999-04-28028 April 1999 Forwards 1998 Annual Environ Operating Rept (Non- Radiological) for Limerick Generating Station,Units 1 & 2. Rept Submitted IAW Section 5.4.1 of App B of Fols,Epp (Non- Radiological) & Describes Implementation of EPP for 1998 ML20206D8801999-04-27027 April 1999 Forwards Rev 2 to LGS Unit 1 Reload 7,Cycle 8 COLR, IAW TS Section 6.9.1.12.COLR Provides cycle-specific Parameter Limits for Noted Info ML20206A5461999-04-21021 April 1999 Responds to Conference Call Between Util & NRC on 990420,re TS Change Request 98-07-2,revising TS Section 2.0 to Incorporate Revised MCPR Safety Limits.Attached Ltr Contains Info Requested ML20205T0441999-04-17017 April 1999 Forwards 1998 Annual Radiological Environ Operating Rept 15, IAW TS Section 6.9.1.7.REMP for 1998,confirmed That LGS Environ Effects from Radioactive Release Were Well Below LGS TSs & Other Applicable Regulatory Limits ML20205Q7581999-04-15015 April 1999 Forwards Response to RAI Re ISI Program First & Second 10-Yr Interval Relief Requests.Revs to Identified by Vertical Bar in Right Margin 1999-09-09
[Table view] Category:LEGAL/LAW FIRM TO NRC
MONTHYEARML20235T8911989-01-18018 January 1989 Forwards Endorsements 130 & 131 to Nelia Policy NF-164, Endorsements 107 & 108 to Maelu Policy MF-44,Endorsements 94 & 95 to Nelia Policy NF-107,Endorsements 110 & 111 to Nelia Policy NF-220 & Endorsements 97 & 98 to Maelu Policy MF-73 ML20196L5401988-07-0505 July 1988 Confirms 880705 Telcon Re Updated Antitrust Review for Facility.Nrc Agrees That Company Has Until 880815 to Respond to Request ML20235B2741987-02-19019 February 1987 FOIA Request for Documents Indicated on Encl Docket Sheets. Request Does Not Encompass Matl Already Available in PDR or Lpdr Denoted by Three or Four Asterisks on List ML20209G1461986-09-0909 September 1986 Requests Issuance of Subpoena for Rt Brown to Testify at Hearing Re Adequacy of Communications Sys Used to Mobilize Manpower Necessary to Evacuate State Correctional Institute in Graterford,Pa ML20214M6501986-09-0909 September 1986 Advises That Licensee Will Not Respond to Air & Water Pollution Patrol 860826 Response to Testimony Re Remand Hearing on Bus Drivers for Oj Roberts & Spring-Ford School Districts,Per Clements .Related Correspondence ML20214M6961986-09-0808 September 1986 Recommends Denial of Rl Anthony 860821 & 25 Petitions for Relief Per 10CFR50.100 & for Ofc of General Counsel Review of NRC 10CFR2.206 Decisions ML20205C4711986-08-0808 August 1986 Forwards 860808 Testimony of Vs Boyer & R Bradshaw Re Remand Hearing on Availability of Bus Drivers for Oj Roberts & Spring-Ford School Districts.Related Correspondence ML20212A7241986-07-24024 July 1986 Notifies That Testimony Presented at 860818 Hearing Will Reflect Revised Number of Volunteer Bus Drivers in Event School Evacuation Necessary ML20211Q1601986-07-21021 July 1986 Advises of Attempts to Deliver Volunteer Sheets of 570 Util Employees Agreeing to Drive Buses in Event of School Evacuation to Limerick Ecology Action (Lea) Headquarters. Related Correspondence ML20206P7421986-06-27027 June 1986 Forwards & Revised Proposed Stipulation in Response to PEMA Request for Changes to Stipulation Re Remanded Issue.Certificate of Svc Encl.Related Correspondence ML20206P9031986-06-26026 June 1986 Corrects Proposing Resolution of Remanded Issue Re Availability of School Bus Drivers for Oj Roberts & Spring-Ford School Districts.Correct Date of Stipulation Re Medical Svcs Is 860616 Instead of 851115 ML20206P7801986-06-25025 June 1986 Responds to AR Love,Counsel for Graterford Inmates,860618 Ltr Accusing Author of Providing ASLB Chairman H Hoyt W/ Trade Publications Re Emergency Planning Requirements. Attempt to Influence Chairman Denied ML20199E5131986-06-19019 June 1986 Forwards Affidavits of AL Bigelow & Vs Boyer Re Availability of Volunteer School Bus Drivers for Oj Roberts & Spring-Ford School Districts in Event of Evacuation,Per ML20199E6881986-06-18018 June 1986 Responds to Re Ex Parte Filing of Offsite Emergency Planning for Nuclear Power Plants:Case of Govt Gridlock. Ex Parte Filings by Rader Seen as Contributing to Lack of Impartiality.Related Correspondence ML20206D7631986-06-16016 June 1986 Forwards Licensee Proposal for Resolution of Remanded Issue Re Availability of School Bus Drivers for Oj Roberts & Spring-Ford School Districts,Per ASLB 860522 Order, Supporting Affidavits & Proposed Stipulation ML20211E7421986-06-11011 June 1986 Forwards Graterford Inmates Response to Aslab 860603 Order. W/O Encl.Related Correspondence ML20198E3721986-05-19019 May 1986 Advises That Excess Flow Check Valves,Described in Dec 1985 License Amend Application Can Be Tested During Plant Operation Using Addl Personnel & Special Procedures.Need for Amend Unaffected.Certificate of Svc Encl ML20197G7961986-05-13013 May 1986 Forwards,For Info,Delaware River Basin in Commission 860427 Revs 5 & 6 to Docket D-69-210 CP Re Dissolved Oxygen Limitations for Temp Constraints & Consumptive Use Allocations.Related Correspondence ML20203P9401986-05-0505 May 1986 Informs That Unit 1 Shut Down on 860502 for Approx 6 Wks During Which All Tests on Excess Flow Check Valves & Other Containment Isolation Valves Will Be Performed.Related Correspondence ML20203E4851986-03-12012 March 1986 FOIA Request for Effluent Rept 3 Submitted Under Encl Ltr. W/O Ltr ML20154L1531986-03-0606 March 1986 Forwards Appeal Board 850805 & Board 831115 Orders & Util to Nrc,Cited in 860219 Answer to Anthony late-filed Petition for Leave to Intervene,Per 860305 Request ML20140D9111986-01-28028 January 1986 Requests Denial of Rl Anthony 860117 Request for Suspension of License & Finding That Util Violated Conditions of License NPF-39 Due to Pending Application for Supplemental Cooling Water Supply ML20154B9491986-01-24024 January 1986 Forwards 851216 Application for Approval of Temporary Substitution of in-stream Monitoring of Dissolved Oxygen Levels in Place of 59 F Constraint on Withdrawals,Filed W/ State of DE River Basin Commission.Related Correspondence ML20138R4571985-12-24024 December 1985 Forwards Procedure M1-18, Decontamination & Treatment of Radioactively Contaminated Patient at Montgomery Hosp. Related Correspondence ML20138R4701985-12-24024 December 1985 Forwards Procedure M1-18, Decontamination & Treatment of Radioactively Contaminated Patient at Montgomery Hosp. Related Correspondence ML20137T2381985-12-16016 December 1985 Advises That 851213 Encl Figures May Be Illegible.Figures Taken Directly from Fsar.W/O Encl.Related Correspondence ML20137U1981985-12-0505 December 1985 Submits Correction to Transcript of Author 851204 Oral Argument on Fourth Partial Initial Decision.Substantive Changes on Pages 47 to 70 Should Be Made ML20136J1971985-11-20020 November 1985 Notifies That Author Will Appear to Present Oral Argument on 851204 on Behalf of Util Re Appeals of Fourth Partial Initial Decision,In Response to 851024 & 1106 Orders.Related Correspondence ML20133L7261985-10-22022 October 1985 Forwards Commonwealth of PA Court Decision Finding Bucks County & Neshaminy Water Resources Authority Obligated to Complete Point Pleasant Project.Related Correspondence ML20133J0491985-10-16016 October 1985 Lists Misspellings & Errors in Transcript of Author 851011 Oral Argument Before Aslab Re Third Partial Initial Decision ML20136C8271985-10-0404 October 1985 Forwards Delaware River Basin Commission 851002 Emergency Certification Granting Application for Use of Schuylkill River Whenever Flow at Pottstown Gage Over 415 Cubic Ft/ Second.Related Correspondence ML20133B0821985-09-30030 September 1985 Informs of Appearance to Present Oral Argument on 851011 Re Appeals of Third Partial Initial Decision in Proceeding,Per 850829 Order.Related Correspondence ML20136A8171985-09-23023 September 1985 Forwards Util Application W/Delaware River Basin Commission for Approval of Withdrawal of Water from Schuylkill River for Consumptive Use & Revised Application Permitting Release from Beachwood Pit.Related Correspondence ML20137Q4971985-09-18018 September 1985 Responds to Mi Lewis Request to Lift or Retract Cp.Petition for Relief Under Section 2.206 Should Be Denied.Puc of PA Recommended Decision Only Basis for Petition ML20137P9411985-09-17017 September 1985 Comments on ALAB-813,including Issuance of Final Findings Not Prerequisite to Authorizing Full Power OL & Error in Curtailing cross-exam Insufficient to Warrant Appellate Relief.Related Correspondence ML20137L4591985-09-0909 September 1985 Advises That Author,Atty for Graterford Inmates,Will Be Unavailable Until 851001.Related Correspondence ML20136A9731985-09-0404 September 1985 Forwards 850813 Notice of Commission Action Approving Application to Delaware River Basin Commission for Approval of Use of Consumptive Water Saved by Curtailment of Listed Plants,Per .Related Correspondence ML20133L8931985-08-0808 August 1985 Forwards Notice of Appeal Re Denial of Stay & Accompanying Memorandum of Law.W/O Encl.Related Correspondence ML20132E3341985-07-30030 July 1985 Informs That Applicant Will Not Respond to Air & Water Pollution Patrol Brief Until 30 Days After Svc of Appeal Brief to Be Filed by Graterford Inmates,Per 850725 Notice of Appeal,Unless Otherwise Directed by Appeal Board ML20126K7831985-07-26026 July 1985 Forwards Comments of Intervenor Graterford Prisoners,Per 850723 Order.W/O Encl.Related Correspondence ML20126L0031985-07-25025 July 1985 Forwards Graterford Inmates Notice of Appeal.W/O Encl. Related Correspondence ML20129C3171985-07-25025 July 1985 Advises That Delaware River Basin Commission Withholding Action on Addl Supplemental Water for Unit 1 Until NRC Authorizes Issuance of Full Power Ol.Requests Action on Full Power License as Soon as Possible ML20137S4861985-07-17017 July 1985 Forwards Util 850603 Application Under Section 3.8 of Delaware River Basin Compact for Use of Water from Beechwood Pit.Related Correspondence ML20128H1591985-07-0303 July 1985 Forwards Testimony of Jd Case.Related Correspondence ML20128F4121985-07-0303 July 1985 Advises of Return of Subpoena to Rl Morris Signed by ASLB on 850628.Morris Gave Deposition Voluntarily at Ofc on 850703 as Result of Arrangements Among Counsel Rather than at Time & Place Listed in Subpoena.Related Correspondence ML20128A2831985-06-28028 June 1985 Requests That ASLB Issue Subpoena Directing Rl Morris to Appear on 850702 in Philadelphia,Pa for Deposition.Rl Morris,Principal Witness Identified by Love on Contention Re Evacuation Time for Graterford.Related Correspondence ML20127L8131985-06-20020 June 1985 Forwards Revised Page 11 to Correct Typo in Applicant Renewed Motion for Exemption from 10CFR50.47(a) Requirements Per Two Contentions Admitted on Behalf of Graterford Prisoners During Litigation Period ML20126J8711985-06-10010 June 1985 Forwards Notice of Delaware River Basin Commission Action Re Temporary Mod to Increase Frequency of Water Withdrawn from Schuylkill River.Some Copies May Have Been Incorrectly Reproduced.Related Correspondence ML20126J7801985-06-0606 June 1985 Forwards 850603 Notice of Commission Action Re Temporary Mod of Delaware River Basin Decision for Facility,As Followup to .Related Correspondence ML20129A6121985-06-0303 June 1985 Forwards,For Info,Application Filed W/Delaware River Basin Commission for Approval for Use During 1985 of Consumptive Use Water Allocations of Titus Units 1,2 & 3 & Cromby Unit 2.Related Correspondence 1989-01-18
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.MR LAW OFFICES 'g CONNER Se WETTERHAHN, P.C.'%RNE8NNoggg 174 7 P E N N S Y LVA NI A AV EN U E. N. W.
TaOv s.CONwEa,Ja. WA S HIN G TO N. .". C. 2 0 0 0 0 MARK J. WETTENHAMN BOBERT M. MADER DOUO1A5 E. OLSON JfSSICA H.1AVERTY w Ls3 xxCHO's . June 6, 19ASETED BOBERT H. PUBL y$hRC (2021 M3-3500 CORNMARD O. BECHHOarER O' ""* 8 ' CABLE ADDRESS; ATOMLAw 85 WN 10 NO:30 GTFtCE OF SELRtW
- 00CKEllHG & StevirJ BRANCH Mr. Samuel J. Chilk Secretary U.S. Nuclear Regulatory Commission -
Washington, D.C. 20555 In the Matter of Philadelphia Electric Company (Limerick Generating Station, Unit 1)
Doc'ket No. 5 0 -3 5 2dL, *
Dear Mr. Chilk:
As a follow-up to my June 3, 1985 letter, I am enclos-ing a Notice of Commission Action dated June 3, 1985 related to a temporary modification of the Delaware River Basin Commission docket decision for the Limerick Generating Station.
Sincerely, ggr f. 0M6 ,
Troy B'. Conner, Jr.
Counsel for the Applicant TBC/dlf Enclosure cc: Service List 8506100695 850606 PDR ADOCK 05000352 G PDR O N
4 DELAWARE RIVER BASIN COMMISSION' WEST T NbN N. 08628 SOCKETED l USHRC l Project Review NOTICE OF COMMISSION ACTION :
Docket NoD 210 CP (Final)(Revise Projact Sponsor: Philadelphia Electric Company-2301 Market Street Philadelphia, Pennsylvania 19101
, Project
Description:
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-Temporary Modification Referred by:
Action by Commission:
Included in the Commission's Comprehensive Plan for the Delaware River Basin and approvedEpursuant to Section 3.8 of the Delaware River Basin Compact. See attached docket for terms and conditions.
Explanatory Note:
This action has been taken by the Commission in accor-dance with its responsibilities under Sections 3.8. 11.1 and 11.2_of the Delaware River Basin Compact. The Commission maintains a comprehensive water resources plan for the Delaware River Basin and reviews water resources projects proposed by other public and private agencies. Review of projects enables the Commission to prevent conflicts among water users and to protect the integrity of the Comprehensive Plan.
YM $ Y Susan M. Weisman, Secretary enc.
cc: R. Timothy Weston; All interested parties CP/3.8
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DOCEET NO. D-69-210 CP (FINAL)(REVISED)
DELAWARE RIVER BASIN C0ttilSSION Philadelphia Electric Company Limerick Electric Generating Station Limerick Township, Montgomery County, Pennsylvania PROCEEDINGS The Philadelphia Electric Company (PECO) applied, on March 21, 1985, for a temporary modification of Docket D-69-210 CP (Final). The application was amended with a submission of supplemental information on April 24, 1985.
The application was reviewed for temporary revision of the project in the Comprehensive Plan and approval of these temporary changes under Section 3.8 of the Delaware River Basin Compact. A public hearing on this applica-tion by PECO was held by the DRBC on May 7, 1985. The hearing record ..
remained open until 5:00 p.m. Ma'y 14, 1985. Sixty-cne co m ats.irere. received
- and entered into the' hearing re'ord c on this application. .
DESCRIPTION Purpose.-- The purpose of this application is to obtain temporary relief, through December 31, 1985, from two existing docket limitations and thereby increase the frequency that water may be withdrawn from the Schuylkill River for evaporation at Limerick Unit No. 1. The two existing limitations are: (1) PECO may not withdraw water from the Schuylkill River for evapgrative use at their Limerick Station when the temperature rises
! above 59 F and (2) water for evaporative use may not be withdrawn from the Schuylkill River when the flow at the Pottstown gage (not augmented by releases from Commission s?onsored reservoir storage) falls below 530 cfs for one Limerick unit in operatio - They requested temporary substitution of DO monitoring to place of temps te restriction in original docket. The l applicant also has requested necessary, release of varying amounts of water not exceeding 32.5 cfs, na water supply storage; and that the con-straint contained in said docket, excluding consideration of releases from Commission-sponsored storage in counting flow at Pottstown, to be inappli-cable to any such releasee.
Location.-- The only change in location of any project facilities is the i proposed location of six dissolved oxygen monitors in lieu of the previously proposed temperature monitor at Pottstown.
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4 D-69-210 CP (FINAL)(REVISED) 3
- b. Facilities.-- All existing facilities of the Limerick Electric Generating Project remain as approved by Docket D-69-210 CP (Final) and the only new facilities required by this application for revision is the addition of the dissolved oxygen monitors.
The requested release of water from existing storage could include existing storage and release facilities, and would not involve any new construction.
Cost.-- The overall cost of the proposed dissolved oxygen monitors is estimated to be $95,000.
Relationship to the Comprehensive Plan.-- The applicant is requesting revision of the Limerick Generating Station Project as included in the Coe-prehensive Plan by Docket D-69-210 CP (Final).
The applicant has also requested that water be released from storage regulated by the Commission whenever docket constraints would otherwise pro-hibit the evaporative use at the Limerick Generating Station. The only storage presently owned and regulated by DRBC in the Schuylkill Basin is storage in Blue Marsh Reservoir. The DRBC Comprehens4ve Plan provisions ,
governing the use of. Blue Marsh Reservoir are included in DRBC Resolution Mo'.
84-7, adopted on April 25, 1984, and also included in Article 2'of the Coe-mission's Water Code of the Delaware River. Basin; Section 2.5.5. Coordinated Operation of Lower Basin and Hydroelectric Reservoirs During a Basinwide Drought.
FINDINGS The Limerick Generating Station was included in the Comprehensive Plan by Docket decision D-69-210 CP (Final) on November 5,1975, which also incor-porated the project description and docket decision D-69-210 CP dated March 29, 1973. Docket D-69-210 CP (5/29/73) includes a section headed
" FINDINGS" subheading " Source of Water Supply 1. Schuylkill River" which reads as follows:
"Schuylkill River water at the plant site may be used for noncon-sumptive use whenever the effluent discharged back to the river meets all applicable water quality standards.
"Schuylkill River water at the plant may be used for consumptive use when flow (not including future augmentations of flow from Commission-sponsored projects) as measured at the Pottstown gage
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is in excess of 530 cfs (342 agd) with one unit in operation and 560 cfs (362 agd) with two units in operation with the following exceptions:
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D-69-210 CP (FINAL)(REVISED) 5 i
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- In a repeat of drought year 1980, substitution of a D0 standard would have permitted Limerick withdrawals only 4 additional days.
- In 1981, use of D0 standard in place of temperature limitation would have allowed Limerick to use Schuylkill water only 5 more 1 days between June and December.
- In 1968 (a normal year), water would have been available for Limerick on 177 days under present temperature and flow con-straints. Substitution of a D0 standard for temperature would have _
allowed water withdrawals 41 more days.
The beneficial impacts to PECO of substituting DO conditioes for the i current temperature restriction during the proposed testing Pror; ram is uncer-
, tain. In its amended application, PECO states:
"Ie conclusion, the effect of the removal of the temperature re striction is uncertain at best, particularly during a drought year; and g g clear.that supplemental. water from storage Q
. -essential. Neverthel'ess, the temperature limitation should be lifted for 1985 and the DO monitoring approach adopted because it appears likely that at least a few days would be ' saved' in 1985 with the corresponding reduction in need for water from storage."
(emphasis added) i 1
On the other hand, during the course of the DRBC hearing, Vincent S.
1 Boyer (PECO Senior Vice President - Nuclear Power) testified that if the DO 4
standards were triggered, plant operations could be suspended rapidly by tripping the reactor shutdown, but reductions "under a controlled manner" would take a matter of 8-10 hours. If DO conditions improved, it would take 10 to 15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br /> to bring the plant back to the power levels prior to shutdown,
- in order to allow the continuation of the testing program.
Mr. Boyer further testified that the test program could be interrupted under certain conditions. The test regimen does not require PECO to operate i Limerick a certain number of days at a continuous level. Certain tests need to be run for a period of time to obtain power calibration data and other information, "but these are generally fairly short number of hours," and the
" test program can be interrupted or adjusted to accommodate the water requirements."
l Exhibits introduced into the hearing record by the DRBC General Cognsel, 4
David Goldberg, (DRBC-1 and DRBC -2) addressed the rationale for the 59 C triggerregtriction. In those exhibits, it is pointed out that DRBC's reason for the 59 C limitation relates to protection c! an :ceptable dissolved i oxygen standard; and further, that higher water temperatures increase the biological demand rate which in turn reduces the dissolved oxygen concentration.
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lt D-69-210 CP (FINAL)(REVISED) 7 In comparison to temperature, which is relatively stable and easy to measure, D0 in river water varies over the day by a fairly wide range. Such variability creates difficulties in setting appropriate trigger criteria, and adjusting power plant operations and water withdrawals on the basis of such changing conditions.
PECO has formally proposed that withdrawal by Limerick for consumptive use be allowed when Pennsylvania water quality standards for DO are not j violated. The applicable standards set forth in 25 Pennsylvania Code Chapter 93 are 5.0 mg/l minimum daily average and 4.0 mg/l minimum instantaneous _
value. In testimony, however, PECO representatives stated that if the -
Company saw that D0 was " trending towards" the 5 mg/l cr 4 as/l standards, it would seek a release of water from Blue Marsh. The Company "could pick a
- value" above the 4 or 5 mg/l levels as a trigger point to request a release, but would "need some experience" to identify such a trigger to protect the D0 standards. The lack of such specificity in the propossi makes even more troublesome the concept of allowing PECO to self-monitor DO and adjust plant operations as it judges appropriate.
Choice o_f_ E Standard: PECO has proposed to base Limerick operations on Pennsylvaniais water quality standards frr the Schuylkill. Other witnesses, however, sugges,ted that more , restrictive standards may be- appropriate to' I
protect fish and aquatic life in the River.
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Philadelphia Suburban Water Company (PSWC) noted that "high temperature l stress increases the sensitivity of aquatic organisms to disease and toxic l pollutants, making the attainment of proper dissolved oxygen criteria par-ticularly important." PSWC recommended the trigger criteria be set according to the National Water Quality Criteria for Dissolved Oxygen. Specifically, the vara water criteria for early life stages is 6.0 mg/l seven day mean and 5.0 mg/l daily concentration. Adoption of such c.riteria would further reduce the number of days in which Limerick could take water from the Schuylkill l without compensation; although a precise calculation of the effect of this revised standard is not available.
Recognizing the special seasonal needs of aquatic life, the Pennsylvania Fish Commission has recommended a two-tiered DO standard for Limerick opera-tions. The Fish Commission proposes that:
"From March 1 to June 15 no water to be withdrawn by Limerick if D.O. values fall below 7 ppa. This is the spawning period for the game species found in the Schuylkill River, and 6-8 ppa of D.O. are necessary to insure successful spawning and incubation for most game species. Flows are usually high enough during this time period so that this D.O. level can be maintained."
"For the remainder of the year the State standards of an average of 5 ppa with no value below 4 ppa would be acceptable providing the lowest readings taken at any of the dans below Limerick are used to determine if the State standards are being met."
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D-69-210 CP (FINAL)(REVISED) 9 j over this 214 day period, assuming continuing drought conditions now being experienced in the Delaware Basin, it is probable that flows on the Schuylkill River during the summer and fall will drop below the 530 cfs trigger for a majority of the time. (In April 1985, the flow on the Schuyl-kill dropped below 530 cfs at one of the earliest times on record, and month-i ly flows set all time new low records - nearly one-third below those experi-i enced during the record drought of 1964-65.) Thus, consumptive use makeup demands upon Blue Marsh of 3000 cis-days or more might be anticipated if the PECO proposal were approved. This quantity would represent 41 percent of the combined water supply and water quality storage in Blue Marsh. 1 PECO estimates of consumptive use needs for Limerick in 1985 are some-what lower. PECO projects a use of 1.5 billion gallons (2322 cis-days) by the end of, October. This would represent 32 percent of the water supply and water quality storage in Blue Marsh. Additional water, of course, would be required to continue operations in November and December.
Under the Basin Comprehensive Plan provisions relating to " Coordinated j Operation of Lower Basin and Hydroelectric Reservoirs During Basinvide
- Drought," Water Code of the Delaware River Basin, Section 2.5.5 (DRBC Reso-lution No. 84-7), the combined storage,of Beltsville,. Blue Mars.h and Nocka-
.- mixon Reservoirs is dedicated.to. provision of releases to augment ri'ver flots
'for salinity control in the Delaware Estuary during periods of basin drought emergency. Operating models developed by DRBC indicate that during a repeat of the drought of record, all of the storage in these three lower basin 2
reservoirs, as well as the New York City reservoirs, would be depleted to meet the requiremects of the drought management plan.
4 l In the DRBC Exhibit #4 entered into the hearing record by Mr. Goldberg, the "DRBC Staff Issues and Response Document; March-April 1984 Public Hear-ing on Proposed Amendment to DRBC Comprehensive Plan Relating to Reservoir Management During Basinwide Drought" dealt with the adverse impacts of evaporating Blue Marsh releases at Limerick:
"Use of releases from storage in the Blue Marsh Project for consumptive use at the Limerick plant would deprive the entire lower Schuylkill River from Limerick to Fairmount Dam of the water quantity and quality benefits which Blue Marsh storage was intended to provide.
"Within this reach of the Schuylkill River frca the Limerick plant to Fairmount Das are eleven water supply withdrawal users, who withdrew 380 mgd in 1982. In this same reach, as of 1982, 28 treated waste discharges contributed 70 med in wastes requiring assimilation and 8,450 lbs./ day BOD5 '"
At any time, the DRBC may call on releases from Blue Marsh Reservoir to enhance poor water quality in the Schuylkill River. If a portion of such
, releases are evaporated off at Limerick, then their diluting effect will be lost to downstrema users.
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D-69-210 CP (FINAL)(REVISED) 11 l
"[T]he temporary short-term use of Blue Marsh should not be precluded simply because drought conditions might arise which require releases from the water supply storage. Under the
' pooled water' concept, drought hardships must be shared equit-ably among all Basin users. Equitable demand upon all impound-ments would be made to meet flow augmentation needs for water supply and water quality in a drought period."
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PECO's argument appears to miss the critical point. Major basin wa'er t
storage is being marshalled under the DRBC drought operations plan to meet I
essential water supply and salinity control needs. Experience and model simulations show that all of this storage may well be exhausted just to meet the requirements of the operating plan in protecting Estuary public water supplies and other existing users.
Moreover, the applicant is seeking the approval to operate under drought conditions when existing docket conditions could preclude the operation even if the Delaware diversion into the Perkiomen Creek project was fully opera-tional and the flow of the Delaware at Trenton was less than 3000 cis.
PECO's proposal..which'would allocate' substantial quantities of water for just one' user, would place an additional draf t on already* stressed resources, and tend to exhaust limited storage even earlier under these drought conditions. The result would be to place downstress water users, J
including those reliant on the Camden and Philadelphia water supply systems, at substantially increased risk.
The DRBC Comprehensive Plan policy on priorities of water use during drought emergencies give first priority to those uses which sustain human life, health and safety (Water Code, Delaware River Basin, Section 2.5.2).
Summary The objective of the 59 temperature limitation contained in the origi-nal docket decision, was to prevent the Limerick project from aggravating dissolved oxygen conditions in the Schuylkill River during critical periods.
The temporary substitution of direct dissolved oxygen monitoring at each critical downstream location is consistent with that objective. In addition, the dissolved oxygen monitors will provide data, not otherwise available to the water resource agencies, for better management of the Schuylkill River.
The temporary use of water from Blue Marsh Reservoir for evaporation at-Limerick Generating Station conflicts with the Comprehensive Plan as cited a bove. Understanding the application is for the remaining portion of 1985, DRBC has considered the application presently before it and recognizes the i seriousness of the current drought emergency already declared by DRBC and l Pennsylvania in making these decisions.
t h D-69-210 CP (FINAL)(REVISED) 13 (3) The provisions set forth in paragraphs (1) and (2) above shall terminate on December 31, 1985, unless otherwise extended or directed by the Commission, and all prior provisions of Docket D-69-210 CP temporarily suspended by this docket shall become operative in full force and effect.
II. The above revisions of the Limerick Nuclear Generating Station project are approved pursuant to Section 3.8 of the Compact, subject to the conditons listed above.
III. The request that DRBC release water from storage at Blue Marsh' Reservoir or other facilic'ies whenever dissolved oxygen limitations or flow limitations would require PECO to replace all evaporative losses at the Limerick Nuclear Generating Station is hereby denied.
BY THE COMMISSION DATED: May 29, 1985
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