ML16039A364

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NRC Integrated Inspection Report 05000282/2015004; 05000306/2015004
ML16039A364
Person / Time
Site: Prairie Island  Xcel Energy icon.png
Issue date: 02/08/2016
From: Kenneth Riemer
NRC/RGN-III/DRP/B2
To: Davison K
Northern States Power Co
References
IR 2015004
Download: ML16039A364 (57)


See also: IR 05000282/2015004

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION III

2443 WARRENVILLE RD. SUITE 210

LISLE, IL 60532-4352

February 8, 2016

Mr. Kevin Davison

Site Vice President

Prairie Island Nuclear Generating Plant

Northern States Power Company, Minnesota

1717 Wakonade Drive East

Welch, MN 55089

SUBJECT: PRAIRIE ISLAND NUCLEAR GENERATING PLANT, UNITS 1

AND 2-NRC INTEGRATED INSPECTION REPORT 05000282/2015004;

05000306/2015004

Dear Mr. Davison:

On December 31, 2015, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Prairie Island Nuclear Generating Plant, Units 1 and 2. The enclosed report

documents the results of this inspection, which were discussed on January 7, 2016, with you,

and other members of your staff.

Based on the results of this inspection, the NRC has identified two issues that were evaluated

under the risk significance determination process as having very low safety significance

(Green). The NRC has also determined that violations are associated with these issues. These

violations are being treated as Non-Cited Violations (NCVs), consistent with Section 2.3.2 of the

Enforcement Policy. Additionally, a licensee-identified violation for which enforcement

discretion was granted is listed in Section 4OA7 of this report.

If you contest the violations or significance of these NCVs, you should provide a response

within 30 days of the date of this inspection report, with the basis for your denial, to the

U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington,

DC 20555-0001, with copies to: (1) the Regional Administrator, Region III; (2) the Director,

Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001;

and (3) the NRC Resident Inspector at the Prairie Island Nuclear Generating Plant.

In addition, if you disagree with the cross-cutting aspect assigned to any finding in this report,

you should provide a response within 30 days of the date of this inspection report, with the basis

for your disagreement, to the Regional Administrator, Region III, and the NRC Resident

Inspector at the Prairie Island Nuclear Generating Plant.

K. Davison -2-

In accordance with Title 10 of the Code of Federal Regulations (CFR) 2.390, Public

Inspections, Exemptions, Requests for Withholding, of the NRC's "Rules of Practice," a copy of

this letter, its enclosure, and your response (if any) will be available electronically for public

inspection in the NRCs Public Document Room or from the Publicly Available Records

System (PARS) component of the NRC's Agencywide Documents Access and Management

System (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Kenneth Riemer

Branch 2

Division of Reactor Projects

Docket Nos. 50-282; 50-306;72-010

License Nos. DPR-42; DPR-60; SNM-2506

Enclosure:

IR 05000282/2015004; 05000306/2015004

cc: Distribution via LISTSERV

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos: 50-282; 50-306;72-010

License Nos: DPR-42; DPR-60; SNM-2506

Report No: 05000282/2015004; 05000306/2015004

Licensee: Northern States Power Company, Minnesota

Facility: Prairie Island Nuclear Generating Plant, Units 1 and 2

Location: Welch, MN

Dates: October 1 through December 31, 2015

Inspectors: L. Haeg, Senior Resident Inspector

P. LaFlamme, Resident Inspector

K. Barclay, Resident Inspector

G. Edwards, Health Physicist

J. Cassidy, Senior Health Physicist

S. Bell, Health Physicist

A. Shaikh, Reactor Inspector

M. Garza, Emergency Preparedness Inspector

Approved by: K. Riemer, Chief

Branch 2

Division of Reactor Projects

Enclosure

TABLE OF CONTENTS

SUMMARY .................................................................................................................................... 2

REPORT DETAILS ....................................................................................................................... 5

Summary of Plant Status ........................................................................................................... 5

1. REACTOR SAFETY ....................................................................................................... 5

1R01 Adverse Weather Protection (71111.01) ............................................................. 5

1R04 Equipment Alignment (71111.04)........................................................................ 6

1R05 Fire Protection (71111.05) .................................................................................. 6

1R06 Flooding (71111.06) ............................................................................................ 7

1R07 Annual Heat Sink Performance (71111.07) ........................................................ 8

1R08 Inservice Inspection Activities (71111.08) ........................................................... 8

1R11 Licensed Operator Requalification Program (71111.11) ................................... 14

1R12 Maintenance Effectiveness (71111.12) ............................................................. 16

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13) ....... 16

1R15 Operability Determinations and Functional Assessments (71111.15) .............. 17

1R18 Plant Modifications (71111.18).......................................................................... 18

1R19 Post-Maintenance Testing (71111.19) .............................................................. 18

1R20 Outage Activities (71111.20) ............................................................................. 19

1R22 Surveillance Testing (71111.22) ....................................................................... 21

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04) ............... 22

1EP6 Drill Evaluation (71114.06) ................................................................................ 22

2. RADIATION SAFETY ................................................................................................... 23

2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01) ............. 23

2RS2 Occupational As-Low-As-Reasonably-Achievable Planning and Controls

(71124.02) ......................................................................................................... 28

2RS5 Radiation Monitoring Instrumentation (71124.05) ............................................. 30

4. OTHER ACTIVITIES ..................................................................................................... 32

4OA1 Performance Indicator Verification (71151)....................................................... 32

4OA2 Identification and Resolution of Problems (71152) ........................................... 35

4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153) .............. 37

4OA5 Other Activities .................................................................................................. 40

4OA6 Management Meetings...................................................................................... 40

4OA7 Licensee-Identified Violations ........................................................................... 41

SUPPLEMENTAL INFORMATION ............................................................................................... 1

Key Points of Contact ................................................................................................................ 1

List of Items Opened, Closed, and Discussed........................................................................... 2

List of Documents Reviewed ..................................................................................................... 3

List of Acronyms Used .............................................................................................................. 9

SUMMARY

Inspection Report 05000282/2015004, 05000306/2015004; 10/01/2015-12/31/2015;

Prairie Island Nuclear Generating Plant, Units 1 and 2; Inservice Inspection Activities; Radiation

Monitoring Instrumentation.

This report covers a 3-month period of inspection by resident inspectors and announced

baseline inspections by regional inspectors. Two Green findings were identified by the

inspectors. The findings involved Non-Cited Violations (NCVs) of U.S. Nuclear Regulatory

Commission (NRC) requirements. The significance of inspection findings was indicated by their

color (i.e., greater than Green, or Green, White, Yellow, Red) and determined using Inspection

Manual Chapter (IMC) 0609, "Significance Determination Process," dated April 29, 2015.

Cross-cutting aspects were determined using IMC 0310, "Aspects Within the Cross-Cutting

Areas," dated December 4, 2014. All violations of NRC requirements are dispositioned in

accordance with the NRCs Enforcement Policy, dated February 4, 2015. The NRC's program

for overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, "Reactor Oversight Process," dated February 2014.

NRC-Identified and Self-Revealed Findings

Cornerstone: Initiating Events

  • Green. The inspectors identified a finding of very low safety significance (Green), and

an associated NCV of Title 10 of the Code of Federal Regulations (CFR) Part 50,

Appendix B, Criterion III, Design Control, for the licensees failure to incorporate the

American National Standards Institute (ANSI) N14.6-1978, Section 5.3.1 required

testing frequency for the reactor vessel head and reactor vessel internals lifting devices

into the controlling preventive maintenance procedure. Compliance with the ANSI

standard was documented in the Safety Evaluation Report (SER) for the licensees

control of heavy loads. The licensee documented the issue in the corrective action

program (CAP) as CAP 01497779 and performed testing on the reactor vessel head and

internals lifting devices during the outage.

The inspectors determined the licensees failure to comply with ANSI N14.6-1978,

Section 5.3.1, for the continued use testing of special lifting devices was a performance

deficiency (PD). The PD was determined to be more-than-minor and a finding because

the PD was associated with the Initiating Events Cornerstone attribute of design control,

and adversely affected the cornerstone objective to limit the likelihood of those events

that upset the plant stability and challenge critical safety functions during shutdown,

as well as power operations. Specifically, compliance with ANSI N14.6-1978,

Section 5.3.1 ensured safe load handling of heavy loads over the reactor core, and/or

over safety-related systems through established testing for the continued functionality of

the special lifting devices. The failure to perform the required frequency of testing on

special lifting devices could increase the likelihood of a load drop and could decrease

the load handling reliability of the lifting device if the device were returned to service with

potentially unacceptable flaws. The inspectors determined the finding could be

evaluated using the Significance Determination Process in accordance with Inspection

Manual Chapter 0609, Significance Determination Process, Attachment 0609.04,

Phase I - Initial Screening and Characterization of Findings, Table 3. Since the finding

was associated with shutdown conditions, the inspectors used Inspection Manual

Chapter 0609, Appendix G, Shutdown Operations Significance Determination Process.

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The inspectors determined that none of the conditions constituting a loss of control were

met, as described in Appendix G, Attachment 1, Phase I Operational Checklists for Both

PWRs [Pressurized Water Reactors] and BWRs [Boiling Water Reactors], for this

finding, and neither a Phase II nor a Phase III analysis was required. Therefore, the

inspectors determined that this finding was of very low safety significance (Green). The

inspectors determined that this finding has a cross-cutting aspect in the area of Human

Performance, Resources, for the licensees failure to ensure that personnel, equipment,

procedures, and other resources were available and adequate to support nuclear safety.

Specifically, the licensee staff evaluated NRC Information Notice (IN) 2014-12, Crane

and Heavy Lift Issues Identified during NRC Inspections, in corrective action program

(CAP) document 01457469. However, in CAP 01457469, the licensee concluded that

issues identified in IN 2014-12 related to other licensees not performing testing in

accordance with ANSI N14.6 requirements were not applicable to the licensee at the

Prairie Island Nuclear Generating Plant. Therefore, the inspectors determined that there

was a recent missed opportunity for the licensee to have reasonably identified that the

current preventive maintenance procedure for special lifting devices was not in

accordance with the ANSI N14.6-1978 requirements, as referenced in the SER. [H.1]

(Section 1R08)

Cornerstone: Public Radiation Safety

  • Green. The inspectors identified a finding of very low safety significance (Green) and

associated NCV of TS 5.5.1.a for the failure to comply with the Offsite Dose Calculation

Manual (ODCM) for not using calibration sources that were traceable to the National

Institute of Standards and Technology (NIST) or equivalent during the calibration of

station effluent monitors. The licensee entered the issues into the CAP as

CAPs 01490581 and 01500149. Immediate corrective actions included the re-calibration

of impacted monitors and the performance of an extent of condition evaluation for other

radiation monitor calibrations.

The PD was determined to be of more than minor safety significance in accordance with

IMC 0612, Appendix B, Issue Screening, dated September 7, 2012, because it was

associated with the plant facilities/equipment and instrumentation attribute of Public

Radiation Safety and it adversely impacted the cornerstone objective of ensuring

adequate protection of public health and safety due to failure to properly calibrate certain

effluent monitors. Subsequent calibrations of the monitors determined that the monitor

efficiency was previously overstated. The inspectors also reviewed IMC 0612,

Appendix E, Examples of Minor Issues, dated August 11, 2009, but did not identify

any similar examples. The finding was assessed using IMC 0609, Appendix D, Public

Radiation Safety Significance Determination Process, dated, February 12, 2008, and

determined to be of very low safety significance (Green), because it was associated with

the effluent release program but was not a failure to implement an effluent program,

public dose did not exceed Appendix I criteria, and the limits in Title 10 CFR 20.1301(e)

were not exceeded. A cross-cutting aspect was not assigned as this issue occurred

numerous years ago. The station has since performed monitor calibrations with

radioactive sources with known quality. (Section 2RS5)

Licensee-Identified Violations

  • Violations of very low safety or security significance or Severity Level IV that were

identified by the licensee have been reviewed by the NRC. Corrective actions taken or

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planned by the licensee have been entered into the licensees corrective action

program (CAP). These violations and CAP tracking numbers are listed in Section 4OA7

of this report.

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REPORT DETAILS

Summary of Plant Status

Unit 1 operated at full power for the entirety of the inspection period, with the exception of brief

down-power maneuvers to accomplish planned surveillance testing activities.

Unit 2 began the inspection period at full power. On October 17, 2015, operations personnel

shut down the Unit 2 reactor to perform Refueling Outage (RFO) 2R29. Major activities

completed during the RFO included replacement of the main generator, main transformer,

containment fan coil unit (FCU) components, 21 reactor coolant pump (RCP) seal, and also

performed steam generator (SG) tube integrity testing. Operations personnel returned the

Unit 2 reactor to operation on December 3, 2015. The main generator was synchronized with

the electrical grid on December 5, 2015.

On December 17, 2015, the Unit 2 main turbine automatically tripped due to a detected

electrical fault within the main generator. This resulted in a reactor trip from 100 percent power.

The licensee began Forced Outage 2F2901HS to address the main generator issue and

remained shutdown in Mode 3 at the end of the inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and

Emergency Preparedness

1R01 Adverse Weather Protection (71111.01)

.1 Winter Seasonal Readiness Preparations

a. Inspection Scope

The inspectors conducted a review of the licensees preparations for winter conditions to

verify that the plants design features and implementation of procedures were sufficient

to protect mitigating systems from the effects of adverse weather. Documentation for

selected risk-significant systems was reviewed to ensure that these systems would

remain functional when challenged by inclement weather. During the inspection, the

inspectors focused on plant specific design features and the licensees procedures used

to mitigate or respond to adverse weather conditions. Additionally, the inspectors

reviewed the Updated Safety Analysis Report (USAR) and performance requirements for

systems selected for inspection, and verified that operator actions were appropriate as

specified by plant specific procedures. Cold weather protection, such as heat tracing

and area heaters, was verified to be in operation where applicable. The inspectors also

reviewed corrective action program (CAP) items to verify that the licensee was

identifying adverse weather issues at an appropriate threshold and entering them into

their CAP in accordance with station corrective action procedures. Documents reviewed

were listed in the Attachment to this report. The inspectors reviews focused specifically

on the following plant systems due to their risk significance or susceptibility to cold

weather issues:

systems.

5

This inspection constituted one winter seasonal readiness preparations sample as

defined in Inspection Procedure (IP) 71111.01-05.

b. Findings

No findings were identified.

1R04 Equipment Alignment (71111.04)

.1 Quarterly Partial System Walkdowns

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

  • Unit 2 train A component cooling (CC) system; and
  • Unit 1 caustic addition system.

The inspectors selected these systems based on their risk significance relative to the

Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted

to identify any discrepancies that could impact the function of the system and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, the USAR, Technical Specification (TS) requirements, outstanding

work orders (WOs), condition reports, and the impact of ongoing work activities on

redundant trains of equipment in order to identify conditions that could have rendered

the systems incapable of performing their intended functions. The inspectors also

walked down accessible portions of the systems to verify system components and

support equipment were aligned correctly and operable. The inspectors examined the

material condition of the components and observed operating parameters of equipment

to verify that there were no obvious deficiencies. The inspectors also verified that the

licensee had properly identified and resolved equipment alignment problems that could

cause initiating events or impact the capability of mitigating systems or barriers and

entered them into the CAP with the appropriate significance characterization.

Documents reviewed are listed in the Attachment to this report.

These inspections constituted three quarterly partial system walkdown samples as

defined in IP 71111.04-05.

b. Findings

No findings were identified.

1R05 Fire Protection (71111.05)

.1 Routine Resident Inspector Tours (71111.05Q)

a. Inspection Scope

The inspectors conducted fire protection walkdowns which were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

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  • Fire Zone 42, Unit 2 reactor building, El. 697' 6";
  • Fire Zone 54, Unit 2 reactor building Unit 2, El. 755';
  • Fire Zone 88, Unit 2 rod control room, El. 735'; and
  • Fire Zone 87, Unit 1 rod control room, El, 735'.

The inspectors reviewed areas to assess if the licensee had implemented a fire

protection program that adequately controlled combustibles and ignition sources within

the plant, effectively maintained fire detection and suppression capability, maintained

passive fire protection features in good material condition, and implemented adequate

compensatory measures for out-of-service, degraded or inoperable fire protection

equipment, systems, or features in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk

as documented in the plants Individual Plant Examination of External Events (IPEEE)

with later additional insights, their potential to impact equipment which could initiate or

mitigate a plant transient, or their impact on the plants ability to respond to a security

event. Using the documents listed in the Attachment to this report, the inspectors

verified that fire hoses and extinguishers were in their designated locations and available

for immediate use; that fire detectors and sprinklers were unobstructed; that transient

material loading was within the analyzed limits; and fire doors, dampers, and penetration

seals appeared to be in satisfactory condition. The inspectors also verified that minor

issues identified during the inspection were entered into the licensees CAP.

Documents reviewed are listed in the Attachment to this report.

These inspections constituted four quarterly fire protection inspection samples as

defined in IP 71111.05-05.

b. Findings

No findings were identified.

1R06 Flooding (71111.06)

.1 Internal Flooding

a. Inspection Scope

The inspectors reviewed selected risk important plant design features and licensee

procedures intended to protect the plant and its safety-related equipment from internal

flooding events. The inspectors reviewed flood analyses and design documents,

including the USAR, engineering calculations, and abnormal operating procedures to

identify licensees commitments. The specific documents reviewed are listed in the

Attachment to this report. In addition, the inspectors reviewed licensees drawings to

identify areas and equipment that may be affected by internal flooding caused by the

failure or misalignment of nearby sources of water, such as the fire suppression or the

circulating water systems. The inspectors also reviewed the licensees corrective action

documents with respect to past flood-related items identified in the corrective action

program to verify the adequacy of the corrective actions. The inspectors performed a

walkdown of the following plant areas to assess the adequacy of watertight doors and

verify drains and sumps were clear of debris and were operable, and that the licensee

complied with its commitments:

  • Unit 1 and 2 AFW system rooms.

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Documents reviewed are listed in the Attachment to this report. This inspection

constituted one internal flooding sample as defined in IP 71111.06-05.

b. Findings

No findings were identified.

1R07 Annual Heat Sink Performance (71111.07)

.1 Heat Sink Performance

a. Inspection Scope

The inspectors reviewed the licensees testing of the Unit 2 train B CC heat exchanger to

verify that potential deficiencies did not mask the licensees ability to detect degraded

performance, to identify any common cause issues that had the potential to increase

risk, and to ensure that the licensee was adequately addressing problems that could

result in initiating events that would cause an increase in risk. The inspectors reviewed

the licensees observations as compared against acceptance criteria, the correlation of

scheduled testing and the frequency of testing, and the impact of instrument

inaccuracies on test results. Inspectors also verified that test acceptance criteria

considered differences between test conditions, design conditions, and testing

conditions. Documents reviewed for this inspection are listed in the Attachment to this

document.

This inspection constituted one annual heat sink performance sample as defined in

IP 71111.07-05.

b. Findings

No findings were identified.

1R08 Inservice Inspection Activities (71111.08)

From October 19, 2015, through November 25, 2015, the inspectors conducted a

review of the implementation of the licensees inservice inspection (ISI) program for

monitoring degradation of the Unit 2 reactor coolant system (RCS), emergency

feedwater systems, risk-significant piping and components, and containment systems.

The reviews described in Sections 1R08.1 through 1R08.5 below constituted one

inservice inspection activities inspection sample as defined in IP 71111.08-05.

.1 Piping Systems Inservice Inspection

a. Inspection Scope

The inspectors reviewed records of the following Non-Destructive Examinations (NDE)

required by the American Society of Mechanical Engineers (ASME)Section XI Code,

and/or Title 10 of the Code of Federal Regulations (CFR) Part 50.55a to evaluate

compliance with the ASME Code,Section XI and V requirements, and if any indications

and defects were detected to determine whether these were dispositioned in accordance

with the ASME Code or an NRC-approved alternative requirement:

8

  • Magnetic Particle Examination of Reactor Vessel Internals Lift Fixture Welds;
  • Magnetic Particle Examination of Reactor Vessel Head Lift Rig Welds;
  • Ultrasonic Examination of Safety Injection Elbow-to-Pipe Weld W-6;
  • Ultrasonic Examination of RH Pipe-to-Elbow Weld W-5;
  • Visual Examination (VT-3) of AFWH-64 Sway Strut/Clamp; and
  • Visual Examination (VT-3) of AFWH-79 Sway Strut/Clamp.

The licensee had not identified any recordable indications during non-destructive surface

and/or volumetric examinations performed since the last RFO. Therefore, no NRC

review was completed for this inspection procedure attribute.

The inspectors reviewed records of the following risk-significant pressure boundary

ASME Code Section XI Class 2 welds fabricated since the beginning of the last

refuelling outage to determine if the licensee: followed the welding procedure;

applied appropriate weld filler material; and implemented the applicable Section XI

or Construction Code NDEs and acceptance criteria. Additionally, the inspectors

reviewed the following welding procedure specification and supporting weld procedure

qualification records to determine if the weld procedure was qualified in accordance

with the requirements of Construction Code and the ASME Code Section XI:

  • Class 1-WO 00406128; Remove and Replace Valve 2RC-7-2, Loop A to

Pressurizer CV-31228 BY-PASS.

b. Findings

Failure to Meet American National Standards Institute N14.6, Section 5.3.1

Requirements

Introduction: The inspectors identified a finding of very low safety significance (Green),

and an associated NCV of Title 10 CFR Part 50, Appendix B, Criterion III, Design

Control, for the licensees failure to incorporate American National Standards Institute

(ANSI) N14.6-1978, Section 5.3.1 required testing frequency for the reactor vessel head

and reactor vessel internals lifting devices into the controlling preventive maintenance

procedure. Compliance with the ANSI standard was documented in the Safety

Evaluation Report (SER) for the licensees control of heavy loads.

Description: The reactor vessel head and reactor vessel internals lifting devices are

classified as safety-related components at Prairie Island. The SER for the Control of

Heavy Loads Phase 1 at Prairie Island Nuclear Generating Plant, Units 1 and 2,

dated June 6, 1983, classified the reactor vessel head and reactor vessel internals

lifting devices as special lifting devices and provided documentation on how compliance

with ANSI N14.6-1978, Standard for Lifting Devices for Shipping Containers Weighing

10,000 Pounds (4500 kg) or more for Nuclear Materials, was met. Specifically,

Section 2.1.5 of the SER stated, in part, the Licensee has indicated that the reactor

vessel head and reactor vessel internals special lifting devices are inspected prior to use

in accordance with the requirements of ANSI N14.6-1978. Such inspection will include

NDE of welds and other critical components. ANSI N14.6-1978, Section 5.3.1 stated,

in part, each special lifting device shall be subjected annually (period not to exceed

14 months) to either of the following:

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  • A load test equal to 150 percent of the maximum load to which the device is to

be subjected; and/or

  • Dimensional testing, visual examination, and NDE of major load-carrying welds

and critical areas. If the device has not been used for a period exceeding one

year, this testing shall not be required. However, in this event, the test shall be

applied before returning the device to service.

The licensee did not perform load testing on these special lifting devices. Further, the

licensee had last performed NDE on these special lifting devices on June 3, 2005,

despite having used them during several outages since.

The inspectors reviewed the licensees preventive maintenance (PM) procedure

PM 3560-52, Reactor Head Lifting Rig Spreader & Connection Legs Assembly

Inspection, Revision 13, and identified that the procedure specified conducting NDE

once during each 10-year interval. The inspectors identified that this site procedure

requirement was contrary to the plant licensing basis as documented in the SER and

ANSI N14.6-1978. The inspectors questioned the licensees basis for decreasing the

required frequency of NDE on the special lifting devices. Specifically, the inspectors

were concerned that failure to perform NDE on the special lifting devices load-carrying

welds at the ANSI N14.6 required frequency potentially challenged continued

functionality of the devices.

The licensee documented the inspectors concerns in CAP 01497779. As part of its

immediate corrective actions, the licensee performed NDE on the reactor vessel head

and reactor vessel internals lifting devices prior to lifting the head and internals during

the outage. As part of additional corrective actions, the licensee intended to revise

procedure PM 3560-52 to correctly translate ANSI N14.6-1978, Section 5.3.1 testing

frequency requirements.

Analysis: The inspectors determined the licensees failure to comply with

ANSI N14.6-1978, Section 5.3.1 for the continued use testing of special lifting devices

was a performance deficiency (PD). The PD was determined to be more-than-minor,

and a finding, because the PD was associated with the Initiating Events Cornerstone

attribute of design control, and adversely affected the cornerstone objective to limit the

likelihood of those events that upset the plant stability and challenge critical safety

functions during shutdown, as well as power operations. Specifically, compliance with

ANSI N14.6-1978, Section 5.3.1, ensured safe load handling of heavy loads over the

reactor core, and/or over safety-related systems through established testing for the

continued functionality of the special lifting devices. The failure to perform the required

frequency of testing on special lifting devices could increase the likelihood of a load drop

and could decrease the load handling reliability of the lifting device if the device were

returned to service with potentially unacceptable flaws.

The inspectors determined the finding could be evaluated using the Significance

Determination Process (SDP) in accordance with Inspection Manual Chapter (IMC)

0609, Significance Determination Process, Attachment 0609.04, Phase I - Initial

Screening and Characterization of Findings, Table 3. Since the finding was associated

with shutdown conditions, the inspectors used IMC 0609, Appendix G, Shutdown

Operations Significance Determination Process. The inspectors determined that none

of the conditions constituting a loss of control were met, as described in Appendix G,

Attachment 1, Phase I Operational Checklists for Both PWRs and BWRs, for this

10

finding, and neither a Phase II nor a Phase III analysis was required. Therefore, the

inspectors determined that this finding was of very low safety significance (Green).

The inspectors determined that this finding has a cross-cutting aspect in the area of

Human Performance, Resources, for the licensees failure to ensure that personnel,

equipment, procedures, and other resources are available and adequate to support

nuclear safety. Specifically, the licensees staff evaluated NRC Information Notice

(IN) 2014-12, Crane and Heavy Lift Issues Identified during NRC Inspections, in CAP

01457469. However, within CAP 01457469, the licensee concluded that issues

identified in IN 2014-12 related to other licensees not performing testing in accordance

with ANSI N14.6 requirements were not applicable to the licensee at the Prairie Island

Nuclear Generating Plant. Therefore, the inspectors determined that there was a recent

missed opportunity for the licensee to have reasonably identified that the current

preventive maintenance procedure for special lifting devices (PM 3560-52) was not in

accordance with the ANSI N14.6-1978 requirements as referenced in the SER. [H.1]

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires,

in part, that measures shall be established to assure that applicable regulatory

requirements and the design basis, as defined in 10 CFR Part 50.2, and as specified in

the license application, for those structures, systems, and components to which this

appendix applies are correctly translated into specifications, drawings, procedures, and

instructions. These measures shall include provisions to assure that appropriate quality

standards are specified and included in design documents and that deviations from such

standards are controlled.

Contrary to the above, since June 3, 2005, the licensee failed to correctly translate its

licensing design basis standard for the control of heavy loads into its PM procedure used

for controlling testing of special lifting devices. Specifically, the licensee failed to

translate the ANSI N14.6-1978 (as required by SER, dated June 6, 1983) testing

frequency requirements for special lifting devices into its controlling PM procedure for

special lifting devices.

The licensee subsequently took immediate corrective actions, which included NDE of

the reactor vessel head and reactor vessel internals lifting devices welds prior to lifting.

Because this violation was of very low safety significance, and it was entered into the

licensees CAP as CAP 01497779, it is being treated as a Non-Cited Violation (NCV),

consistent with Section 2.3.2 of the NRC Enforcement Policy

(NCV 05000306/2015004-01, Failure to Meet ANSI N14.6 Section 5.3.1

Requirements).

.2 Reactor Pressure Vessel Upper Head Penetration Inspection Activities

a. Inspection Scope

For the Unit 2 reactor vessel head, no examinations (visual or non-visual) were

required this outage pursuant to 10 CFR 50.55a(g)(6)(ii)(D) requirements. Therefore,

no examination was conducted by the licensee and no NRC review was completed for

this inspection procedure attribute.

b. Findings

No findings were identified.

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.3 Boric Acid Corrosion Control

a. Inspection Scope

The inspectors independently walked down the Unit 2 reactor coolant system loop

piping, including the reactor coolant pumps, pressurizer, and emergency core cooling

systems within containment to identify boric acid leakage. The inspectors then reviewed

the walkdown performed by the licensee to ensure that components with boric acid

deposits were identified and entered into the CAP. The inspectors observed these

examinations to determine whether the licensee focused on locations where boric

acid leaks can cause degradation of safety significant components.

The inspectors reviewed the following licensee evaluations of components with boric

acid deposits to determine if the affected components were documented and properly

evaluated in the corrective action system. Specifically, the inspectors evaluated the

following CAP documents to determine if degraded components met the component

Construction Code and/or the ASME Section XI Code:

Indication on CV-31325;

  • CAP 01450480; BACC Evaluation for ISI Indication on RC-19-1;
  • CAP 01450476; BACC Evaluation for ISI Indication on 135-011; and
  • CAP 01427328; BACC Evaluation for Leak Identified in Unit 2 Containment 21

Vault.

The inspectors reviewed the following CAP documents related to evidence of boric

acid leakage to determine whether the corrective actions completed were consistent with

the requirements of the ASME Code Section XI and 10 CFR Part 50, Appendix B,

Criterion XVI:

  • CAP 01412727; Leak From Capped Drain Downstream of 2RC-8-19;
  • CAP 01492989; Boric Acid Built Up Below 21 Safety Injection Pump; and
  • CAP 01445383; 22 Safety Injection Pump IB/OB Mechanical Seal Leakage.

b. Findings

No findings were identified.

.4 Steam Generator Tube Inspection Activities

a. Inspection Scope

The NRC inspectors observed acquisition of ET data, interviewed ET data personnel,

and reviewed documentation related to the SG ISI program to determine if:

  • in-situ SG tube pressure testing screening criteria used were consistent with

those identified in the Electric Power Research Institute (EPRI) TR-107620,

Steam Generator In-Situ Pressure Test Guidelines, and that these criteria were

properly applied to screen degraded SG tubes for in-situ pressure testing;

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  • the numbers and sizes of SG tube flaws/degradation identified were bound by

the licensees previous outage Operational Assessment predictions;

  • the SG tube ET examination scope and expansion criteria were sufficient to meet

the TSs and EPRI 1003138, Pressurized Water Reactor SG Examination

Guidelines;

  • the SG tube ET examination scope included potential areas of tube degradation

identified in prior outage SG tube inspections and/or as identified in NRC generic

industry operating experience applicable to these SG tubes;

  • the licensee identified new tube degradation mechanisms and implemented

adequate extent of condition inspection scope and repairs for the new tube

degradation mechanism;

  • the licensee implemented repair methods which were consistent with the repair

processes allowed in the plant TS requirements and to determine if qualified

depth sizing methods were applied to degraded tubes accepted for continued

service;

  • the licensee implemented an inappropriate plug on detection tube repair

threshold (e.g., no attempt at sizing of flaws to confirm tube integrity);

  • the licensees primary-to-secondary leakage (e.g., SG tube leakage) was below

3 gallons-per-day or the detection threshold during the previous operating cycle;

  • the ET probes and equipment configurations used to acquire data from the

SG tubes were qualified to detect the known/expected types of SG tube

degradation in accordance with Appendix H, Performance Demonstration for

ET Examination of EPRI 1003138, Pressurized Water Reactor SG Examination

Guidelines;

  • the licensee performed secondary side SG inspections for location and removal

of foreign materials; and

  • the licensee implemented repairs for SG tubes damaged by foreign material.

The licensee did not perform in-situ pressure testing of SG tubes. Therefore, no NRC

review was completed for this inspection attribute.

b. Findings

No findings were identified.

.5 Identification and Resolution of Problems

a. Inspection Scope

The inspectors performed a review of ISI/SG-related problems entered into the

licensees CAP, and conducted interviews with licensees staff to determine if:

  • the licensee had established an appropriate threshold for identifying

ISI/SG-related problems;

  • the licensee had performed a root cause (if applicable) and taken appropriate

corrective actions; and

  • the licensee had evaluated operating experience and industry generic issues

related to ISI and pressure boundary integrity.

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The inspectors performed these reviews to evaluate compliance with 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Action, requirements. The corrective action

documents reviewed by the inspectors are listed in the Attachment to this report.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program (71111.11)

.1 Resident Inspector Quarterly Review of Licensed Operator Requalification (71111.11Q)

a. Inspection Scope

On October 6, 2015, the inspectors observed a crew of licensed operators in the plants

simulator during licensed operator requalification training. The inspectors verified that

operator performance was adequate, evaluators were identifying and documenting crew

performance problems, and that training was being conducted in accordance with

licensee procedures. The inspectors evaluated the following areas:

  • licensed operator performance;
  • crews clarity and formality of communications;
  • ability to take timely actions in the conservative direction;
  • prioritization, interpretation, and verification of annunciator alarms;
  • correct use and implementation of abnormal and emergency procedures;
  • control board manipulations;
  • oversight and direction from supervisors; and
  • ability to identify and implement appropriate TS actions and Emergency Plan

actions and notifications.

The crews performance in these areas was compared to pre-established operator action

expectations and successful critical task completion requirements. Documents reviewed

are listed in the Attachment to this report.

This inspection constituted one quarterly licensed operator requalification program

simulator sample as defined in IP 71111.11-05 and satisfied the inspection program

requirement for the resident inspectors to observe a portion of an in-progress annual

requalification operating test during a training cycle in which it was not observed by the

NRC during the biennial portion of this IP.

b. Findings

No findings were identified.

.2 Resident Inspector Quarterly Observation during Periods of Heightened Activity or Risk

(71111.11Q)

a. Inspection Scope

On October 16, 2015, the inspectors observed the Unit 2 shutdown activities in

preparation for the Unit 2 RFO. These were activities that required heightened

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awareness or were related to increased risk. The inspectors evaluated the following

areas:

  • licensed operator performance;
  • crews clarity and formality of communications;
  • ability to take timely actions in the conservative direction;
  • prioritization, interpretation, and verification of annunciator alarms;
  • correct use and implementation of procedures;
  • control board manipulations; and
  • oversight and direction from supervisors.

The performance in these areas was compared to pre-established operator action

expectations, procedural compliance and task completion requirements. Documents

reviewed are listed in the Attachment to this report.

This inspection constituted one quarterly licensed operator heightened activity/risk

sample as defined in IP 71111.11-05.

b. Findings

No findings were identified.

.3 Resident Inspector Quarterly Observation during Periods of Heightened Activity or Risk

(71111.11Q)

a. Inspection Scope

On December 3, 2015, the inspectors observed the Unit 2 control room startup activities.

These were activities that required heightened awareness or were related to increased

risk. The inspectors evaluated the following areas:

  • licensed operator performance;
  • crews clarity and formality of communications;
  • ability to take timely actions in the conservative direction;
  • prioritization, interpretation, and verification of annunciator alarms;
  • correct use and implementation of procedures;
  • control board manipulations; and
  • oversight and direction from supervisors.

The performance in these areas was compared to pre-established operator action

expectations, procedural compliance and task completion requirements. Documents

reviewed are listed in the Attachment to this report.

This inspection constituted one quarterly licensed operator heightened activity/risk

sample as defined in IP 71111.11-05.

b. Findings

No findings were identified.

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1R12 Maintenance Effectiveness (71111.12)

.1 Routine Quarterly Evaluations

a. Inspection Scope

The inspectors evaluated the following:

  • Unit 1 CC system; and

The inspectors reviewed events such as where ineffective equipment maintenance had

resulted in valid or invalid automatic actuations of engineered safeguards systems and

independently verified the licensee's actions to address system performance or condition

problems in terms of the following:

  • implementing appropriate work practices;
  • identifying and addressing common cause failures;
  • scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
  • characterizing system reliability issues for performance;
  • charging unavailability for performance;
  • trending key parameters for condition monitoring;
  • verifying appropriate performance criteria for structures, systems, and

components (SSCs)/functions classified as (a)(2), or appropriate and adequate

goals and corrective actions for systems classified as (a)(1).

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified that

maintenance effectiveness issues were entered into the CAP with the appropriate

significance characterization. Documents reviewed are listed in the Attachment to this

report.

This inspection constituted two quarterly maintenance effectiveness samples as defined

in IP 71111.12-05.

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

.1 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for the

maintenance and emergent work activities affecting risk-significant and safety-related

equipment listed below to verify that the appropriate risk assessments were performed

prior to removing equipment for work:

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  • loss of Unit 1 & 2 emergency response computer system (ERCS) on

November 17 & 18, 2015;

  • failure of a re-heat drain tank valve resulting in a thermal power increase on

November 19, 2015; and

  • emergent examination of reactor special lift devices and resulting extended

duration at reduced inventory.

These activities were selected based on their potential risk significance relative to the

Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that

risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate

and complete. When emergent work was performed, the inspectors verified that the

plant risk was promptly reassessed and managed. The inspectors reviewed the scope

of maintenance work, discussed the results of the assessment with the licensee's

probabilistic risk analyst or shift technical advisor, and verified plant conditions were

consistent with the risk assessment. The inspectors also reviewed TS requirements and

walked down portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met.

Documents reviewed during this inspection are listed in the Attachment to this report.

These maintenance risk assessments and emergent work control activities constituted

three samples as defined in IP 71111.13-05.

b. Findings

No findings were identified.

1R15 Operability Determinations and Functional Assessments (71111.15)

.1 Operability Evaluations

a. Inspection Scope

The inspectors reviewed the following issue:

  • CAP 01500184, Unit 1 AFW Recirculation Line Operability Evaluation.

The inspectors selected this potential operability issue based on the risk significance of

the associated components and systems. The inspectors evaluated the technical

adequacy of the evaluation to ensure that TS operability was properly justified and the

subject components or systems remained available such that no unrecognized increase

in risk occurred. The inspectors compared the operability and design criteria in the

appropriate sections of the TS and USAR to the licensees evaluation to determine

whether the components or systems were operable. Where compensatory measures

were required to maintain operability, the inspectors determined whether the measures

in place would function as intended and were properly controlled. The inspectors

determined, where appropriate, compliance with bounding limitations associated with the

evaluation. Additionally, the inspectors reviewed a sampling of corrective action

documents to verify that the licensee was identifying and correcting any deficiencies

associated with operability evaluation. Documents reviewed are listed in the Attachment

to this report.

This operability inspection constituted one sample as defined in IP 71111.15-05.

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b. Findings

No findings were identified.

1R18 Plant Modifications (71111.18)

.1 Plant Modifications

a. Inspection Scope

The inspectors reviewed the following modification:

  • Unit 2 turbine building crane load capacity uprate.

The inspectors reviewed the configuration changes and associated 10 CFR 50.59 safety

evaluation screening against the design basis, the USAR, and the TS, as applicable, to

verify that the modification did not affect the operability or availability of the

affected/impacted systems. The inspectors, as applicable, observed ongoing and

completed work activities to ensure that the modifications were installed as directed and

consistent with the design control documents; the modifications operated as expected;

post-modification testing adequately demonstrated continued system operability,

availability, and reliability; and that operation of the modifications did not impact the

operability of any interfacing systems. As applicable, the inspectors verified that relevant

procedure, design, and licensing documents were properly updated. Lastly, the

inspectors discussed the plant modification with operations, engineering, and training

personnel to ensure that the individuals were aware of how the operation with the plant

modification in place could impact overall plant performance. Documents reviewed are

listed in the Attachment to this report.

This inspection constituted one permanent plant modification sample as defined in

IP 71111.18-05.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing (71111.19)

.1 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed the following post maintenance activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

  • cooling water supply to 121 safeguards traveling water screen solenoid valve

replacement;

  • 21 RCP testing following seal replacement; and

maintenance activities.

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These activities were selected based upon the structure, system, or component's ability

to impact risk. The inspectors evaluated these activities for the following (as applicable):

the effect of testing on the plant had been adequately addressed; testing was adequate

for the maintenance performed; acceptance criteria were clear and demonstrated

operational readiness; test instrumentation was appropriate; tests were performed as

written in accordance with properly reviewed and approved procedures; equipment was

returned to its operational status following testing (temporary modifications or jumpers

required for test performance were properly removed after test completion); and test

documentation was properly evaluated. The inspectors evaluated the activities against

TSs, the USAR, 10 CFR Part 50 requirements, licensee procedures, and various

NRC generic communications to ensure that the test results adequately ensured that the

equipment met the licensing basis and design requirements. In addition, the inspectors

reviewed corrective action documents associated with post-maintenance tests to

determine whether the licensee was identifying problems and entering them in the CAP

and that the problems were being corrected commensurate with their importance to

safety. Documents reviewed are listed in the Attachment to this report.

These inspections constituted three post-maintenance testing samples as defined in

IP 71111.19-05.

b. Findings

No findings were identified.

1R20 Outage Activities (71111.20)

.1 Refueling Outage Activities

a. Inspection Scope

The inspectors reviewed the Outage Safety Plan (OSP) and contingency plans for

the Unit 2 RFO conducted October 17, 2015, through December 5, 2015, to confirm

that the licensee had appropriately considered risk, industry experience, and previous

site-specific problems in developing and implementing a plan that assured maintenance

of defense-in-depth. During the RFO, the inspectors observed portions of the shutdown

and cooldown processes and monitored licensee controls over the outage activities

listed below:

  • licensee configuration management, including maintenance of defense-in-depth

commensurate with the OSP for key safety functions, and compliance with the

applicable TS when taking equipment out of service;

  • implementation of clearance activities and confirmation that tags were properly

hung and equipment appropriately configured to safely support the work or

testing;

  • installation and configuration of reactor coolant pressure, level, and temperature

instruments to provide accurate indication, accounting for instrument error;

  • controls over the status and configuration of electrical systems to ensure that

TS and OSP requirements were met, and controls over switchyard activities;

  • controls to ensure that outage work was not impacting the ability of the operators

to operate the spent fuel pool cooling system;

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alternative means for inventory addition, and controls to prevent inventory loss;

  • controls over activities that could affect reactivity;
  • licensee fatigue management, as required by 10 CFR 26, Subpart I;
  • refueling activities, including fuel handling and sipping to detect fuel assembly

leakage;

  • startup and ascension to full power operation, tracking of startup prerequisites,

walkdown of the drywell (primary containment) to verify that debris had not been

left which could block emergency core cooling system suction strainers, and

reactor physics testing; and

  • licensee identification and resolution of problems related to RFO activities.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted one RFO sample as defined in IP 71111.20-05.

b. Findings

No findings were identified.

.2 Other Outage Activities

a. Inspection Scope

The inspectors evaluated outage activities for an unscheduled outage that began on

December 17, 2015, and continued through the remainder of the inspection period. The

inspectors reviewed activities to ensure that the licensee considered risk in developing,

planning, and implementing the outage schedule.

The inspectors observed or reviewed portions of the reactor trip and associated action

taken in response the Unit 2 main generator trip, which caused an automatic turbine and

subsequent reactor trip. Additionally, the inspectors observed and reviewed outage

equipment configuration and risk management, electrical lineups, selected clearances,

control and monitoring of decay heat removal, control of containment activities,

personnel fatigue management, and identification and resolution of problems associated

with the outage. As of December 31, 2015, the cause of the main generator trip and

resultant automatic turbine and reactor trip was still under investigation. Because the

unscheduled outage was ongoing at the end of the inspection period, this inspection did

not constitute a complete other outage activities sample, as defined in IP 71111.20-05.

b. Findings

No findings were identified.

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1R22 Surveillance Testing (71111.22)

.1 Surveillance Testing

a. Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether

risk-significant systems and equipment were capable of performing their intended safety

function and to verify testing was conducted in accordance with applicable procedural

and TS requirements:

  • SP 2083A, Unit 2 Integrated SI [Safety Injection] Test with a Simulated Loss of

Offsite Power Train A, Revision 4 (inservice testing).

The inspectors observed in-plant activities and reviewed procedures and associated

records to determine the following:

  • did preconditioning occur;
  • the effects of the testing were adequately addressed by control room personnel

or engineers prior to the commencement of the testing;

  • acceptance criteria were clearly stated, demonstrated operational readiness, and

were consistent with the system design basis;

  • plant equipment calibration was correct, accurate, and properly documented;
  • as-left setpoints were within required ranges; and the calibration frequency was

in accordance with TSs, the USAR, procedures, and applicable commitments;

  • measuring and test equipment calibration was current;
  • test equipment was used within the required range and accuracy; applicable

prerequisites described in the test procedures were satisfied;

  • test frequencies met TS requirements to demonstrate operability and reliability;

tests were performed in accordance with the test procedures and other

applicable procedures; jumpers and lifted leads were controlled and restored

where used;

  • test data and results were accurate, complete, within limits, and valid;
  • test equipment was removed after testing;
  • where applicable for inservice testing activities, testing was performed in

accordance with the applicable version of Section XI, American Society of

Mechanical Engineers code, and reference values were consistent with the

system design basis;

  • where applicable, test results that did not meet acceptable criteria were

addressed with an adequate operability evaluation or the system or component

was declared inoperable;

  • where applicable for safety-related instrument control surveillance tests,

reference setting data were accurately incorporated in the test procedure;

  • where applicable, actual conditions encountering high resistance electrical

contacts were such that the intended safety function could still be accomplished;

  • prior procedure changes had not provided an opportunity to identify problems

encountered during the performance of the surveillance or calibration test;

  • equipment was returned to a position or status required to support the

performance of its safety functions; and

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  • all problems identified during the testing were appropriately documented and

dispositioned in the CAP.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted one inservice test sample as defined in IP 71111.22,

Sections-02 and-05.

b. Findings

No findings were identified.

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)

.1 Emergency Action Level and Emergency Plan Changes

a. Inspection Scope

Regional inspectors performed an in-office review of the latest revisions to the

Emergency Plan, Emergency Action Levels (EAL), and EAL Bases document to

determine if these changes decreased the effectiveness of the Emergency Plan.

The inspectors also performed a review of the licensees 10 CFR Part 50.54(q) change

process, and Emergency Plan change documentation to ensure proper implementation

for maintaining Emergency Plan integrity.

The NRC review was not documented in an SER and did not constitute approval of

licensee-generated changes; therefore, this revision is subject to future inspection. The

specific documents reviewed during this inspection are listed in the Attachment to this

report.

This inspection constituted one EAL and Emergency Plan change sample as defined in

Inspection Procedure 71114.04-05.

b. Findings

No findings were identified.

1EP6 Drill Evaluation (71114.06)

.1 Training Observation

a. Inspection Scope

The inspectors observed a simulator training evolution for licensed operators on

October 6, 2015, which required emergency plan implementation by a licensee

operations crew. This evolution was planned to be evaluated and included in

performance indicator data regarding drill and exercise performance. The inspectors

observed event classification and notification activities performed by the crew. The

inspectors also attended the post-evolution critique for the scenario. The focus of the

inspectors activities was to note any weaknesses and deficiencies in the crews

performance and ensure that the licensee evaluators noted the same issues and entered

them into the corrective action program. As part of the inspection, the inspectors

22

reviewed the scenario package and other documents listed in the Attachment to this

report.

This inspection constituted one training evolution with emergency preparedness drill

aspects sample as defined in IP 71114.06-06.

b. Findings

No findings were identified.

2. RADIATION SAFETY

Cornerstones: Occupational and Public Radiation Safety

2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01)

These inspection activities supplement those documented in IR 05000282/2015002;

05000306/2015002, and constituted one complete radiological hazard assessment and

exposure controls sample as defined in IP 71124.01-05.

.1 Inspection Planning (02.01)

a. Inspection Scope

The inspectors reviewed all licensee performance indicators (PIs) for the Occupational

Exposure Cornerstone for follow-up. The inspectors reviewed the results of radiation

protection program audits (e.g., licensees quality assurance audits or other independent

audits). The inspectors reviewed any reports of operational occurrences related to

occupational radiation safety since the last inspection. The inspectors reviewed the

results of the audit and operational report reviews to gain insights into overall licensee

performance.

b. Findings

No findings were identified.

.2 Radiological Hazard Assessment (02.02)

a. Inspection Scope

The inspectors determined if there have been changes to plant operations since the last

inspection that resulted in significant new radiological hazards for onsite workers or

members of the public. The inspectors evaluated whether the licensee assessed the

potential impact of these changes and has implemented periodic monitoring, as

appropriate, to detect and quantify the radiological hazard(s).

The inspectors reviewed the last two radiological surveys from selected plant areas and

evaluated whether the thoroughness and frequency of the surveys were appropriate for

the given radiological hazard(s).

The inspectors conducted walkdowns of the facility, including radioactive waste

processing, storage, and handling areas to evaluate material conditions and performed

independent radiation measurements to verify conditions.

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The inspectors selected the following radiologically risk-significant work activities that

involved exposure to radiation:

  • 10-year ISI/corrosion inspection-2R29;
  • scaffold standard work-U2 outage; and

For these work activities, the inspectors assessed whether the pre-work surveys

performed were appropriate to identify and quantify the radiological hazard and to

establish adequate protective measures. The inspectors evaluated the radiological

survey program to determine if hazards were properly identified, including the following:

  • identification of hot particles;
  • the presence of alpha emitters;
  • the potential for airborne radioactive materials, including the potential presence

of transuranic and/or other hard-to-detect radioactive materials (this evaluation

may have included licensee planned entry into non-routinely entered areas

subject to previous contamination from failed fuel);

  • the hazards associated with work activities that could suddenly and severely

increase radiological conditions and that the licensee had established a means to

inform workers of changes that could have significantly impacted their

occupational dose; and

  • severe radiation field dose gradients that could have resulted in non-uniform

exposures of the body.

The inspectors observed work in potential airborne areas and evaluated whether the air

samples were representative of the breathing air zone. The inspectors evaluated

whether continuous air monitors were located in areas with low background to minimize

false alarms and were representative of actual work areas. The inspectors evaluated

the licensees program for monitoring levels of loose surface contamination in areas of

the plant with the potential for the contamination to become airborne.

b. Findings

No findings were identified.

.3 Instructions to Workers (02.03)

a. Inspection Scope

The inspectors selected various containers that held non-exempt, licensed radioactive

materials that could have caused unplanned or inadvertent exposure of workers, and

assessed whether the containers were labeled and controlled in accordance with

10 CFR 20.1904, Labeling Containers, or met the requirements of 10 CFR 20.1905(g),

Exemptions To Labeling Requirements.

The inspectors reviewed the following radiation work permits (RWPs) used to access

high-radiation areas and evaluated the specified work control instructions or control

barriers:

24

  • RWP 155021, 10-Year ISI/Corrosion Inspection-2R29;
  • RWP 152055, Scaffold Standard Work-U2 Outage; and

For these RWPs, the inspectors assessed whether allowable stay times or permissible

dose (including from the intake of radioactive material) for radiologically significant work

under each RWP were clearly identified. The inspectors evaluated whether electronic

personal dosimeter alarm set-points were in conformance with survey indications and

plant policies. The inspectors reviewed selected occurrences where a workers

electronic personal dosimeter noticeably malfunctioned or alarmed. The inspectors

evaluated whether workers responded appropriately to the off-normal condition. The

inspectors assessed whether the issues were included in the CAP and dose evaluations

were conducted as appropriate.

For work activities that could suddenly and severely increase radiological conditions, the

inspectors assessed the licensees means to inform workers of changes that could

significantly impact their occupational dose.

b. Findings

No findings were identified.

.4 Contamination and Radioactive Material Control (02.04)

a. Inspection Scope

The inspectors observed locations where the licensee monitored potentially

contaminated material leaving radiological controlled areas and inspected the methods

used for control, survey, and release from these areas. The inspectors observed the

performance of personnel surveying and releasing material for unrestricted use and

evaluated whether the work was performed in accordance with plant procedures and

whether the procedures were sufficient to control the spread of contamination and

prevent unintended release of radioactive materials from the site. The inspectors

assessed whether the radiation monitoring instrumentation had appropriate sensitivity for

the type(s) of radiation present.

The inspectors reviewed the licensees criteria for the survey and release of potentially

contaminated material. The inspectors evaluated whether there was guidance on how to

respond to an alarm that indicated the presence of licensed radioactive material.

The inspectors reviewed the licensees procedures and records to verify that radiation

detection instrumentation was used at its typical sensitivity level based on appropriate

counting parameters. The inspectors assessed whether or not the licensee had

established a de facto release limit by altering the instruments typical sensitivity

through such methods as raising the energy discriminator level or locating the instrument

in a high-radiation background area.

The inspectors selected several sealed sources from the licensees inventory records

and assessed whether the sources were accounted for and verified to be intact.

The inspectors evaluated whether any transactions, since the last inspection, involving

nationally tracked sources were reported in accordance with 10 CFR 20.2207.

25

b. Findings

No findings were identified.

.5 Radiological Hazards Control and Work Coverage (02.05)

a. Inspection Scope

The inspectors evaluated ambient radiological conditions (e.g., radiation levels or

potential radiation levels) during tours of the facility. The inspectors assessed whether

the conditions were consistent with applicable posted surveys, RWPs, and worker

briefings.

The inspectors evaluated the adequacy of radiological controls, such as required

surveys, radiation protection job coverage (including audio and visual surveillance for

remote job coverage), and contamination controls. The inspectors evaluated the

licensees use of electronic personal dosimeters in high-noise areas as high-radiation

area monitoring devices.

The inspectors assessed whether radiation monitoring devices were placed on the

individuals body consistent with licensee procedures. The inspectors assessed whether

the dosimeter was placed in the location of highest expected dose or that the licensee

properly employed an NRC-approved method of determining effective dose equivalent.

The inspectors reviewed the application of dosimetry to effectively monitor exposure to

personnel in high-radiation work areas with significant dose rate gradients.

The inspectors reviewed the following RWPs for work within airborne radioactivity areas

with the potential for individual worker internal exposures:

  • RWP 155021; 10-Year ISI/Corrosion Inspection-2R29;
  • RWP 152055; Scaffold Standard Work-U2 Outage; and

For these RWPs, the inspectors evaluated airborne radioactive controls and monitoring,

including potential for significant airborne levels (e.g., grinding, grit blasting, system

breaches, and entry into tanks, cubicles, and reactor cavities). The inspectors assessed

barrier (e.g., tent or glove box) integrity and temporary high-efficiency particulate air

ventilation system operation.

The inspectors examined the licensees physical and programmatic controls for

highly activated or contaminated materials (i.e., nonfuel) stored within spent fuel

and other storage pools. The inspectors assessed whether appropriate controls

(i.e., administrative and physical controls) were in place to preclude inadvertent

removal of these materials from the pool.

The inspectors examined the posting and physical controls for selected high-radiation

areas and very-high radiation areas to verify conformance with the occupational PI.

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b. Findings

No findings were identified.

.6 Risk-Significant High-Radiation Area and Very-High Radiation Area Controls (02.06)

a. Inspection Scope

The inspectors discussed the controls in place for special areas that had the potential to

become very-high radiation areas during certain plant operations with first-line health

physics supervisors (or equivalent positions having backshift health physics oversight

authority). The inspectors assessed whether these plant operations required

communication beforehand with the health physics group, so as to allow corresponding

timely actions to properly post, control, and monitor the radiation hazards including

re-access authorization.

b. Findings

No findings were identified.

.7 Radiation Worker Performance (02.07)

a. Inspection Scope

The inspectors observed performance of radiation workers with respect to stated

radiation protection work requirements. The inspectors assessed whether workers were

aware of the radiological conditions in their workplace and the RWP controls/limits in

place, and whether their performance reflected the level of radiological hazards present.

The inspectors reviewed radiological-related CAPs since the last inspection that found

the cause of the event to be human performance errors. The inspectors evaluated

whether there was an observable pattern traceable to a similar cause. The inspectors

assessed whether this perspective matched the corrective action approach taken by the

licensee to resolve the reported problems. The inspectors discussed with the radiation

protection manager any problems with the corrective actions that were planned or that

were taken.

b. Findings

No findings were identified.

.8 Radiation Protection Technician Proficiency (02.08)

a. Inspection Scope

The inspectors observed the performance of the radiation protection technicians with

respect to radiation protection work requirements. The inspectors evaluated whether

technicians were aware of the radiological conditions in their workplace and the RWP

controls/limits, and whether their performance was consistent with their training and

qualifications with respect to the radiological hazards and work activities.

The inspectors reviewed radiological-related CAPs since the last inspection that found

the cause of the event to be radiation protection technician error. The inspectors

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evaluated whether there was an observable pattern traceable to a similar cause. The

inspectors assessed whether this perspective matched the corrective action approach

taken by the licensee to resolve the reported problems.

b. Findings

No findings were identified.

.9 Problem Identification and Resolution (02.09)

a. Inspection Scope

The inspectors evaluated whether problems associated with radiation monitoring and

exposure control were being identified by the licensee at an appropriate threshold and

whether they were properly addressed for resolution in the licensees CAP. The

inspectors assessed the appropriateness of the corrective actions for a selected sample

of problems documented by the licensee that involved radiation monitoring and exposure

controls. The inspectors assessed the licensees process for applying operating

experience at the facility.

b. Findings

No findings were identified.

2RS2 Occupational As-Low-As-Reasonably-Achievable Planning and Controls (71124.02)

These inspection activities supplement those documented in IR 05000282/2014002;

05000306/2014002, and constitute one complete occupational as-low-as-reasonably-

achievable (ALARA) planning and controls sample as defined in IP 71124.02-05.

.1 Radiological Work Planning (02.02)

a. Inspection Scope

The inspectors selected the following work activities of the highest exposure

significance:

  • RWP 155021; 10-Year ISI/Corrosion Inspection-2R29;
  • RWP 152055; Scaffold Standard Work-U2 Outage; and

The inspectors reviewed the ALARA work activity evaluations, exposure estimates, and

exposure mitigation requirements. The inspectors determined whether the licensee

reasonably grouped the radiological work into work activities based on historical

precedence, industry norms, and/or special circumstances.

The inspectors assessed whether the licensees planning identified appropriate dose

mitigation features, considered alternate mitigation features, and defined reasonable

dose goals. The inspectors evaluated whether the licensees ALARA assessments had

taken into account decreased worker efficiency from use of respiratory protective

devices and/or heat stress mitigation equipment (e.g., ice vests). The inspectors

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determined whether the licensees work planning considered the use of remote

technologies (e.g., teledosimetry, remote visual monitoring, and robotics) as a means to

reduce dose and the use of dose reduction insights from industry operating experience

and plant-specific lessons learned. The inspectors assessed the integration of ALARA

requirements into work procedure and RWP documents.

The inspectors compared the results achieved (dose rate reductions and person-rem

used) with the intended dose established in the licensees ALARA planning for these

work activities. The inspectors compared the person-hour estimates provided by

maintenance planning and other groups to the radiation protection group with the actual

work activity time requirements and evaluated the accuracy of these time estimates.

The inspectors assessed the reasons (e.g., failure to adequately plan the activity and

failure to provide sufficient work controls) for any inconsistencies between intended and

actual work activity doses.

The inspectors determined whether post-job reviews were conducted and if identified,

problems were entered into the licensees CAP.

b. Findings

No findings were identified.

.2 Verification of Dose Estimates and Exposure Tracking Systems (02.03)

a. Inspection Scope

The inspectors reviewed the assumptions and bases (including dose rate and man-hour

estimates) for the current annual collective exposure estimate for reasonable accuracy

for select ALARA work packages. The inspectors reviewed applicable procedures to

determine the methodology for estimating exposures from specific work activities and

the intended dose outcome.

b. Findings

No findings were identified.

.3 Source Term Reduction and Control (02.04)

a. Inspection Scope

The inspectors used licensee records to determine the historical trends and current

status of significant tracked plant source terms known to contribute to elevated facility

aggregate exposure. The inspectors assessed whether the licensee had made

allowances or developed contingency plans for expected changes in the source term as

the result of changes in plant fuel performance issues or changes in plant primary

chemistry.

b. Findings

No findings were identified.

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.4 Radiation Worker Performance (02.05)

a. Inspection Scope

The inspectors observed the performance of radiation workers and radiation protection

technicians during work activities within in radiation areas, airborne radioactivity areas,

and/or high-radiation areas. The inspectors evaluated whether workers demonstrated

the ALARA philosophy in practice (e.g., workers were familiar with the work activity

scope and tools to be used, workers used ALARA low-dose waiting areas), and whether

there were any procedure compliance issues (e.g., workers were not complying with

work activity controls). The inspectors observed the performance of radiation workers to

assess whether training and skill levels were sufficient with respect to the radiological

hazards and the work involved.

b. Findings

No findings were identified.

2RS5 Radiation Monitoring Instrumentation (71124.05)

These inspection activities supplement those documented in IR 05000282/2014002;

05000306/2014002 and constituted one complete radiation monitoring instrumentation

sample as defined in IP 71124.05-05.

.1 Calibration and Testing Program (02.03)

Process and Effluent Monitors

a. Inspection Scope

The inspectors selected effluent monitor instruments (such as gaseous and liquid) and

evaluated whether channel calibration and functional tests were performed consistent

with radiological effluent TS/ODCM requirements. The inspectors assessed whether:

(a) the licensee calibrated its monitors with National Institute of Standards and

Technology (NIST) traceable sources; (b) the primary calibrations adequately

represented the plant nuclide mix; (c) when secondary calibration sources were used,

the sources were verified by the primary calibration; and (d) the licensees channel

calibrations encompassed the instruments alarm setpoints.

The inspectors assessed whether the effluent monitor alarm setpoints were established

as provided in the ODCM and station procedures.

For changes to effluent monitor setpoints, the inspectors evaluated the basis for

changes to ensure that an adequate justification existed.

b. Findings

Failure to Adequately Calibrate Liquid Effluent Monitors

Introduction: The inspectors identified a finding of very low safety significance (Green)

and associated NCV of TS 5.5.1.a for the failure to comply with the ODCM for not using

calibration sources, which were traceable to the NIST or equivalent during the calibration

of station effluent monitors.

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Description: The inspectors reviewed the primary calibration records for various station

effluent monitors. These calibrations included the Unit 2 SG blowdown effluent monitor

(2R-19) and the waste effluent liquid monitor (R-18), which were both performed on

April 7, 1993. Primary calibrations are normally performed after monitor installation or

major maintenance. The purpose of primary calibrations is to determine the in-situ or

installed effluent monitor efficiency. Subsequent secondary calibrations are then

performed periodically, as specified by the ODCM, to ensure monitor response is

unchanged. During the inspection, the inspectors determined that the radioactive

sources used for these calibrations did not contain any quality information, such as NIST

or equivalent traceability. This issue of concern was then entered into the licenses CAP

on August 20, 2015. Subsequently, the licensee performed new primary calibrations

with a set of radioactive sources with an established quality. The new calibrations

resulted in a reduced efficiency when compared to the previous calibrations, which was

outside of the stations acceptance criteria. Although the new calibration efficiency was

lower, this did not require changes to the monitor alarm setpoints.

Analysis: The inspectors determined that not utilizing NIST traceable calibration sources

(or equivalent) during the primary calibration of the station effluent monitors was a PD,

the cause of which was reasonably within the licensees ability to foresee and correct,

and should have been prevented. The finding was not subject to traditional enforcement

since the incident did not result in a significant safety consequence, did not impact the

NRCs ability to perform its regulatory function, and was not willful.

The PD was determined to be of more than minor safety significance in accordance with

IMC 0612, Appendix B, Issue Screening, dated September 7, 2012, because it was

associated with the plant facilities/equipment and instrumentation attribute of Public

Radiation Safety and it adversely impacted the objective of ensuring adequate protection

of public health and safety due to failure to properly calibrate certain effluent monitors.

Subsequent calibration of the monitors determined that the monitor efficiency was

previously overstated. The inspectors also reviewed IMC 0612, Appendix E, Examples

of Minor Issues, dated August 11, 2009, but did not identify any similar examples. The

finding was assessed using IMC 0609, Appendix D, Public Radiation Safety

Significance Determination Process, dated February 12, 2008, and determined to be of

very low safety significance (Green) because it was associated with the effluent release

program but was not a failure to implement an effluent program, public dose did not

exceed Appendix I criteria, and the limits in 10 CFR 20.1301(e) were not exceeded. A

cross-cut aspect was not assigned as this issue occurred numerous years ago. The

station has since performed monitor calibrations with radioactive sources with known

quality. An example was the Unit 1 SG blowdown effluent monitor, which was calibrated

on August 25, 2015.

Enforcement: Technical Specification 5.5.1.a states, in part, that the ODCM shall

contain the methodology and parameters used in the calculation of offsite doses. The

ODCM Table 2.3, Radioactive Liquid Effluent Monitoring Instrumentation, Surveillance

Requirements, specifies, in part, that initial channel calibrations be performed with

NIST certified or NIST traceable sources.

Contrary to the above, on April 7, 1993, 2R-19 and R-18 were not calibrated with NIST

certified, NIST traceable, or other suitable quality radioactive source(s). Corrective

actions included the re-calibration of these monitors and an extent of condition on

additional effluent monitors. Since the finding was of very low safety significance

31

(Green) and was entered into the licensees CAP as CAPs 01490581 and 01500149,

this violation is being treated as an NCV consistent with Section 2.3.2 of the NRC

Enforcement Policy (NCV 05000282/2015004-02, Failure to Adequately Calibrate

Liquid Effluent Monitors).

4. OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and

Security

4OA1 Performance Indicator Verification (71151)

.1 Mitigating Systems Performance IndexEmergency AC Power System

a. Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index (MSPI)-Emergency AC Power System PI, Units 1 and 2, for the period from the

4th quarter of 2014 through the 3rd quarter of 2015. To determine the accuracy of the PI

data reported during those periods, PI definitions and guidance contained in the Nuclear

Energy Institute (NEI) Document 99-02, Regulatory Assessment Performance Indicator

Guideline, Revision 7, dated August 31, 2013, were used. The inspectors reviewed the

licensees operator narrative logs, MSPI derivation reports, issue reports, event reports

and NRC integrated IRs for the period of October of 2014 through September of 2015 to

validate the accuracy of the submittals. The inspectors reviewed the MSPI component

risk coefficient to determine if it had changed by more than 25 percent in value since the

previous inspection, and if so, that the change was in accordance with applicable

NEI guidance. The inspectors also reviewed the licensees issue report database to

determine if any problems had been identified with the PI data collected or transmitted

for this indicator and none were identified. Documents reviewed are listed in the

Attachment to this report.

This inspection constituted two MSPI emergency AC power system samples as defined

in IP 71151-05.

b. Findings

No findings were identified.

.2 Mitigating Systems Performance IndexResidual Heat Removal System

a. Inspection Scope

The inspectors sampled licensee submittals for the MSPI - RHR System PI, Units 1 and

2, for the period from the 4th quarter of 2014 through the 3rd quarter of 2015. To

determine the accuracy of the PI data reported during those periods, PI definitions and

guidance contained in the NEI Document 99-02, Regulatory Assessment Performance

Indicator Guideline, Revision 7, dated August 31, 2013, were used. The inspectors

reviewed the licensees operator narrative logs, MSPI derivation reports, issue reports,

event reports and NRC integrated IRs for the period of October of 2014 through

September of 2015 to validate the accuracy of the submittals. The inspectors reviewed

32

the MSPI component risk coefficient to determine if it had changed by more than 25

percent in value since the previous inspection, and if so, that the change was in

accordance with applicable NEI guidance. The inspectors also reviewed the licensees

issue report database to determine if any problems had been identified with the PI data

collected or transmitted for this indicator and none were identified. Documents reviewed

are listed in the Attachment to this report.

This inspection constituted two MSPI residual heat removal system samples as defined

in IP 71151-05.

b. Findings

No findings were identified.

.3 Mitigating Systems Performance IndexCooling Water Systems

a. Inspection Scope

The inspectors sampled licensee submittals for the MSPI-CL Systems PI,

Units 1 and 2, for the period from the 4th quarter of 2014 through the 3rd quarter of

2015. To determine the accuracy of the PI data reported during those periods, PI

definitions and guidance contained in the NEI Document 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were

used. The inspectors reviewed the licensees operator narrative logs, MSPI derivation

reports, issue reports, event reports and NRC integrated IRs for the period of October of

2014 through September of 2015 to validate the accuracy of the submittals. The

inspectors reviewed the MSPI component risk coefficient to determine if it had changed

by more than 25 percent in value since the previous inspection, and if so, that the

change was in accordance with applicable NEI guidance. The inspectors also reviewed

the licensees issue report database to determine if any problems had been identified

with the PI data collected or transmitted for this indicator and none were identified.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted two MSPI cooling water system samples as defined in

IP 71151-05.

b. Findings

No findings were identified.

.4 Reactor Coolant System Specific Activity

a. Inspection Scope

The inspectors sampled licensee submittals for the RCS Specific Activity PI for the

period from the 4th quarter of 2014 through the 3rd quarter of 2015. The inspectors

used PI definitions and guidance contained in the NEI Document 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, to

determine the accuracy of the PI data reported during those periods. The inspectors

reviewed the licensees RCS chemistry samples, technical specification requirements,

issue reports, event reports and NRC Integrated IRs to validate the accuracy of the

submittals. The inspectors also reviewed the licensees issue report database to

33

determine if any problems had been identified with the PI data collected or transmitted

for this indicator. In addition to record reviews, the inspectors observed a chemistry

technician obtain and analyze a RCS sample. Documents reviewed are listed in the

Attachment to this report.

This inspection constituted two RCS specific activity samples as defined in IP 71151-05.

b. Findings

No findings were identified.

.5 Occupational Exposure Control Effectiveness

a. Inspection Scope

The inspectors sampled licensee submittals for the Occupational Exposure

Control Effectiveness PI for the period from the 4th quarter of 2014 through the

3rd quarter of 2015. The inspectors used PI definitions and guidance contained in

the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline,

Revision 7, dated August 31, 2013, to determine the accuracy of the PI data reported

during those periods. The inspectors reviewed the licensees assessment of the PI

for occupational radiation safety to determine if indicator related data was adequately

assessed and reported. To assess the adequacy of the licensees PI data collection and

analyses, the inspectors discussed with radiation protection staff, the scope and breadth

of its data review and the results of those reviews. The inspectors independently

reviewed electronic personal dosimetry dose rate, accumulated dose alarms, and dose

reports, and the dose assignments for any intakes that occurred during the time period

reviewed to determine if there were potentially unrecognized occurrences. The

inspectors also conducted walkdowns of numerous locked high and very-high radiation

area entrances to determine the adequacy of the controls in place for these areas.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted one occupational exposure control effectiveness sample as

defined in IP 71151-05.

b. Findings

No findings were identified.

.6 Radiological Effluent Technical Specification/Offsite Dose Calculation Manual

Radiological Effluent Occurrences

a. Inspection Scope

The inspectors sampled licensees submittals for the Radiological Effluent Technical

Specification (RETS)/ODCM Radiological Effluent Occurrences PI for the period from

the 4th quarter of 2014 through the 3rd quarter of 2015. The inspectors used PI

definitions and guidance contained in the NEI Document 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, to

determine the accuracy of the PI data reported during those periods. The inspectors

reviewed the licensees CAP database and selected individual reports generated since

this indicator was last reviewed to identify any potential occurrences such as

34

unmonitored, uncontrolled, or improperly calculated effluent releases that may have

impacted offsite dose. The inspectors reviewed gaseous effluent summary data and the

results of associated offsite dose calculations for selected dates to determine if indicator

results were accurately reported. The inspectors also reviewed the licensees methods

for quantifying gaseous and liquid effluents and determining effluent dose. Documents

reviewed are listed in the Attachment to this report.

This inspection constituted one RETS/ODCM radiological effluent occurrences sample

as defined in IP 71151-05.

b. Findings

No findings were identified.

4OA2 Identification and Resolution of Problems (71152)

.1 Routine Review of Items Entered into the Corrective Action Program

a. Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

and plant status reviews to verify they were being entered into the licensees CAP at an

appropriate threshold, that adequate attention was being given to timely corrective

actions, and that adverse trends were identified and addressed. Attributes reviewed

included: identification of the problem was complete and accurate; timeliness was

commensurate with the safety significance; evaluation and disposition of performance

issues, generic implications, common causes, contributing factors, root causes,

extent-of-condition reviews, and previous occurrences reviews were proper and

adequate; and that the classification, prioritization, focus, and timeliness of corrective

actions were commensurate with safety and sufficient to prevent recurrence of the issue.

Minor issues entered into the licensees CAP as a result of the inspectors observations

are included in the Attachment to this report.

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by procedure, they were considered an

integral part of the inspections performed during the quarter and documented in

Section 1 of this report.

b. Findings

No findings were identified.

.2 Daily Corrective Action Program Reviews

a. Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for follow-up, the inspectors performed a daily screening of

items entered into the licensees CAP. This review was accomplished through

inspection of the stations daily condition report packages.

35

These daily reviews were performed by procedure as part of the inspectors daily plant

status monitoring activities and, as such, did not constitute any separate inspection

samples.

b. Findings

No findings were identified.

.3 Semi-Annual Trend Review

a. Inspection Scope

The inspectors performed a review of the licensees CAP and associated documents to

identify trends that could indicate the existence of a more significant safety issue. The

inspectors review was focused on repetitive equipment issues, but also considered the

results of daily inspector CAP item screening discussed in Section 4OA2.2, licensee

trending efforts, and licensees human performance results. The inspectors review

nominally considered the 6-month period of July of 2015 through December of 2015,

although some examples expanded beyond those dates where the scope of the trend

warranted.

The review also included issues documented outside the normal CAP in major

equipment problem lists, repetitive and/or rework maintenance lists, departmental

problem/challenges lists, system health reports, quality assurance audit/surveillance

reports, self-assessment reports, and Maintenance Rule assessments. The inspectors

compared and contrasted their results with the results contained in the licensees

CAP trending reports. Corrective actions associated with a sample of the issues

identified in the licensees trending reports were reviewed for adequacy.

This review constituted one semi-annual trend inspection sample as defined in

IP 71152-05.

b. Findings

No findings were identified.

.4 Annual Follow-up of Selected Issues: CAP 01494532; Safety-Related Relay for Reactor

Protection System Service Life Evaluation

a. Inspection Scope

During a review of items entered in the licensees CAP, the inspectors noted that

CAPs 01493179 and 01493183 documented safety related relays installed in the reactor

protection system had surpassed the vendor qualified life of 20 years. In their review,

the inspectors identified that the CAPs listed above did not address the impact of

exposure to low humidity conditions present during the late fall and winter months. In

response, the licensee performed a detailed evaluation under CAP 01494532 to

document the impact of low humidity on electrical equipment. The inspectors reviewed

the associated evaluation and also the procedures associated with humidity monitoring

and noted that per CAP 01495083, issued on September 29, 2015, the service building

computer room containing the ERCS reached the low humidity alarm set point and

annunciated. The inspector discussed this noted condition with operations staff and it

36

was recognized that the same alarm had annunciated in the fall of 2014. Based on the

above information, the inspectors reviewed associated CAPs and work requests that had

been generated since September of 2014 that addressed low humidity indications

present during the late fall and winter months in 2014 and 2015, respectively. The

inspectors determined that the evaluation performed under CAP 01494532 adequately

addressed the impact of low humidity on electrical components and noted that the

licensee planned to replace all applicable relays during the next RFOs for each Unit.

The inspectors noted that the associated relays addressed in CAP 01494532 remained

operable but non-conforming and therefore remained capable of performing their

required safety functions.

This review constituted one in-depth problem identification and resolution sample as

defined in IP 71152-05.

b. Findings

No findings were identified.

4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153)

.1 Unit 2 Automatic Reactor Trip and Notice of Unusual Event

a. Inspection Scope

On December 17, 2015, Unit 2 experienced an automatic reactor trip resulting from an

automatic turbine shutdown caused by a main generator lockout. The inspectors

responded to the control room and monitored the operator actions taken to address the

event. Following the trip, the control room received unexpected fire alarms within the

Unit 2 containment. A Notice of Unusual Event was declared but subsequently exited

after the licensee verified that no fire existed within containment. The inspectors

reviewed the procedures used during this event to determine whether the control room

operators responded properly. Documents reviewed are listed in the Attachment to this

report.

This review constituted one event follow-up sample as defined in IP 71153-05.

b. Findings

No findings were identified.

.2 (Closed) Licensee Event Report 05000282/2014-002-00 and-01: Emergency Diesel

Generators Declared Inoperable Due to Not Meeting High Energy Line Break

Requirements

a. Inspection Scope

On August 4, 2014, the licensee submitted the above Licensee Event Report (LER) to

the NRC to document a condition that could have prevented the fulfillment of the D1 and

D2 EDGs safety function. The condition, identified on June 3, 2014, was associated

with a calculated turbine building (TB) high energy line break (HELB) heat-up analysis

temperature that exceeded the maximum supply and exhaust fan blade positioner

temperatures for the D1 and D2 EDGs. The licensee declared both D1 and D2

37

inoperable, entered the applicable TS action statements, and implemented

compensatory measures to bypass the supply and exhaust fan blade positioners to full

cooling mode allowing the station to exit the applicable TS action statements.

The licensee initiated a CAP and root cause evaluation that was still in progress at the

LER submittal deadline, therefore, on January 30, 2015, the licensee submitted

supplement-01 to the above LER which described the final root cause and corrective

actions.

Following submittal of the above LER supplement, the licensee received testing data

from a third party vendor that demonstrated acceptable operation of the supply and

exhaust fan blade positioners at the elevated temperatures identified within the TB HELB

calculation. Therefore, on July 23, 2015, the licensee submitted a cancellation letter to

NRC for LERs 05000282/2014-002-00 and-01 since the original condition did not result

in the prevention of the fulfillment of the D1 and D2 EDGs safety function.

The inspectors reviewed the revised analysis and the cancellation letter. No concerns

were identified. Documents reviewed are listed in the Attachment to this report. This

LER is closed.

This review constituted one event follow-up sample as defined in IP 71153-05.

b. Findings

No findings were identified.

.3 (Closed) LER 05000282/2015-001-00: 14 Fan Coil Unit Leak

a. Inspection Scope

On January 16, 2015, the licensee submitted the above LER to the NRC to document a

condition that could have prevented the fulfillment of the Unit 1 containment safety

function. The condition, identified on November 20, 2014, with Unit 1 in Mode 3, was

associated with a cooling water leak from the 14 containment fan coil unit (FCU) that

impacted containment integrity. The licensee declared the Unit 1 containment

inoperable, entered the applicable TS LCO statement, and isolated the 14 containment

FCU within the Unit 1 containment TS action completion time allowing the station to exit

the applicable TS action statement. Repairs were conducted shortly thereafter and the

14 containment FCU was returned to service.

Following submittal of the above LER, the licensee performed an engineering evaluation

that demonstrated that containment leakage past the auxiliary building special ventilation

zone and shield building would have remained less than the available containment

leakage margin. Therefore, since the 14 containment FCU leak did not represent a

condition that could have prevented the fulfillment of the Unit 1 containment safety

function, the licensee submitted a cancellation letter to NRC for

LER 05000282/2015-001-00 on September 3, 2015.

The inspectors reviewed the revised analysis and the cancellation letter. No concerns

were identified. Documents reviewed are listed in the Attachment to this report. This

LER is closed.

38

This review constituted one event follow-up sample as defined in IP 71153-05.

b. Findings

No findings were identified.

.4 (Closed) LER 05000282/2015-002-00: 14 Fan Coil Unit Leak (Lower Head)

a. Inspection Scope

On April 10, 2015, the licensee submitted the above LER to the NRC to document a

condition that could have prevented the fulfillment of the Unit 1 containment safety

function. The condition, identified on February 10, 2015, with Unit 1 in Mode 3, was

associated with a cooling water leak from the 14 containment FCU that impacted

containment integrity. The licensee declared the Unit 1 containment inoperable, entered

the applicable TS action statement, and implemented repairs to the 14 containment FCU

within the Unit 1 containment TS action completion time allowing the station to exit the

applicable TS action statement.

Following submittal of the above LER, the licensee performed an engineering evaluation

(see Section 4OA3.3) that demonstrated that containment leakage past the auxiliary

building special ventilation zone and shield building would have remained less than the

available containment leakage margin. Therefore, since the 14 containment FCU leak

did not represent a condition that could have prevented the fulfillment of the Unit 1

containment safety function, the licensee submitted a cancellation letter to NRC for LER

05000282/2015-002-00 on September 3, 2015.

The inspectors reviewed the revised analysis and the cancellation letter. No concerns

were identified. Documents reviewed are listed in the Attachment to this report. This

LER is closed.

This review constituted one event follow-up sample as defined in IP 71153-05.

b. Findings

No findings were identified.

.5 (Closed) LER 05000282/2015-003-00: Unanalyzed Condition Due to Non-Compliance

with 10 CFR 50 Appendix R

a. Inspection Scope

The inspectors reviewed information provided by the licensee regarding the

April 19, 2015, identification of inadequate procedure steps within procedure

F5 Appendix B, Control Room Evacuation (Fire), Revision 31. Specifically, during a

National Fire Protection Association (NFPA) 805 transition process review of

Engineering Change 25405, 12 Reactor Cooling Pump Seal Face Replacement, the

licensee identified that F5 Appendix B did not contain required procedural steps to open

direct current (DC) knife switches for the 11, 12, 21, and 22 RCP breakers prior to

evacuation of the control/relay and cable spreading rooms during a postulated fire event

in those areas. The unanalyzed condition was associated with the potential for fire

induced circuit damage resulting in RCP(s) restarting without adequate seal cooling

39

restored, leading to seal failure and a small break loss of coolant accident. The

unanalyzed condition only impacted the 12 RCP since the 11, 21, and 22 RCPs had

appropriately modified seals to allow time for restoring seal cooling prior to seal failure.

During the inspection, the inspectors reviewed the fire protection program documents,

licensees CAPs, the apparent cause evaluation, immediate corrective actions (F5

Appendix B procedure change), and longer term corrective actions. Documents

reviewed are listed in the Attachment to this report. This LER is closed.

This review constituted one event follow-up sample as defined in IP 71153-05.

b. Findings

One finding and NCV for which the NRC exercised enforcement discretion was identified

during the review of this LER. The inspectors determined that the finding and NCV

associated with the unanalyzed condition was best characterized as a licensee identified

finding and violation. As a result, the inspectors documented information regarding this

issue in Section 4OA7 of this inspection report.

4OA5 Other Activities

.1 Institute of Nuclear Power Operations Plant Assessment Report Review

a. Inspection Scope

The inspectors reviewed the final report for the Institute of Nuclear Power Operations

(INPO) plant evaluation conducted in September and October of 2015. The inspectors

reviewed the report to ensure that issues identified were consistent with the NRC

perspectives of licensees performance and to verify if any significant safety issues were

identified that required further NRC follow-up.

b. Findings

No findings were identified.

4OA6 Management Meetings

.1 Exit Meeting Summary

On January 7, 2016, the inspectors presented the inspection results to Mr. K. Davison,

Site Vice President, and other members of the staff. The licensee acknowledged the

issues presented. The inspectors confirmed that none of the potential report input

discussed was considered proprietary.

.2 Interim Exit Meetings

Interim exits were conducted for:

40

  • The inspection results for the areas of radiological hazard assessment and

exposure controls; occupational ALARA planning and controls; and RCS specific

activity, occupational exposure control effectiveness, and RETS/ODCM

radiological effluent occurrences PI verification with Mr. K. Klotz, Acting Radiation

Protection Manager, on November 6, 2015;

  • The results of the ISI inspection with Mr. M. Pearson, Regulatory Affairs

Manager, and other members of the licensee staff on November 25, 2015;

  • The inspection results for the area of radiation monitoring instrumentation via

teleconference, with Mr. D. Gauger, Chemistry Manager, on December 28, 2015;

and

Emergency Preparedness Manager, Mr. B. Carberry, Emergency Preparedness

Manager, via telephone on December 21, 2015.

The inspectors confirmed that none of the potential report input discussed was

considered proprietary. Proprietary material received during the inspection was returned

to the licensee.

4OA7 Licensee-Identified Violations

The following violation of very low safety significance (Green) was identified by the

licensee. The NRC is not taking enforcement action for this violation because it met the

criteria of the NRC Enforcement Policy, "Interim Enforcement Policy Regarding

Enforcement Discretion for Certain Fire Protection Issues (10 CFR 50.48)," as described

below:

to operate before January 1, 1979, must satisfy the applicable requirements of

Appendix R to this part, including specifically the requirements of Sections III.G,

III.J, and III.O. Appendix R,Section III.G.3 of 10 CFR Part 50, requires, in part,

that alternative or dedicated shutdown capability and its associated circuits,

independent of cables, systems or components in the area, room, or zone under

consideration should be provided where the protection of systems whose

function is required for hot shutdown does not satisfy the requirement of

paragraph G.2 of this section. In addition, fire detection and a fixed fire

suppression system shall be installed in the area, room, or zone under

consideration.

Contrary to the above, on April 19, 2015, the licensee failed to ensure that

alternative or dedicated shutdown capability and its associated circuits were

independent of cables in the area. Specifically, procedure F5 Appendix B,

Control Room Evacuation (Fire), Revision 31, did not contain actions to isolate

the RCP breaker circuits to prevent restarting due to a fire induced loss of remote

trip and loss of RCP seal cooling water that could lead to an increased rate of

seal degradation and a small break loss of coolant accident. These actions were

required to achieve and maintain safe shutdown in the event of a fire that

resulted in functional loss and/or evacuation of the control/relay and cable

spreading rooms.

Section 9.1 of the NRC Enforcement Policy allows the NRC to exercise

enforcement discretion for certain fire protection related non compliances

41

identified as a result of a licensees transition to the new risk informed,

performance based fire protection approach included in 10 CFR 50.48(c), and for

certain existing non compliances that reasonably may be resolved by compliance

with 10 CFR 50.48(c) as long as certain criteria are met. This risk informed,

performance based approach is referred to as NFPA 805, Performance Based

Standard for Fire Protection for Light Water Reactor Electric Generating Plants.

The licensee is in transition to NFPA 805 and therefore the licensee-identified

violation was evaluated in accordance with the criteria established by Section

9.1(a) of the NRCs Interim Enforcement Policy Regarding Enforcement

Discretion for Certain Fire Protection Issues (10 CFR 50.48) for a licensee in

NFPA 805 transition. The inspectors determined that for this violation: (1) the

licensee would have identified the violation during the scheduled transition to 10

CFR 50.48(c); (2) the licensee had established adequate compensatory

measures within a reasonable time frame following identification and would

correct the violation as a result of completing the NFPA 805 transition; (3) the

violation was not likely to have been previously identified by routine licensee

efforts; and (4) the violation was not willful. The finding also met additional

criteria established in section 12.01.b of IMC 0305, Operating Assessment

Program. In addition, in order for the NRC to consider granting enforcement

discretion the violation must not be associated with a finding of high safety

significance (i.e., Red).

The licensee performed risk evaluation V.SPA.15.012, Revision 3, dated

December 18, 2015, and determined that this issue was not associated with a

finding of high safety significance. A region III senior reactor analyst (SRA)

reviewed the evaluation and concluded that the result was reasonable and that

the finding was less than Red and eligible for enforcement discretion. The

dominant core damage sequence from the licensees evaluation involved an

electrical cabinet fire in the relay room involving the cables that could cause

spurious operation of the RCPs and that would lead to alternate shutdown. The

licensee identified several conservative assumptions in the analysis. The SRA

agreed that some were conservative, notably that any fire affecting the cables in

the relay room that could cause a spurious start of an RCP would also result in a

loss of all seal cooling due to fire damage. The SRA used IMC 0609, Appendix

F, Fire Protection Significance Determination Process, to review the results of

the licensees evaluation. The relay room is similar to a cable spreading room

with electrical cabinets. The fire frequency for this room in Appendix F is

6E-3/yr. The probability of non-suppression was estimated to be 2E-2 and the

spurious operation probability was assumed to be 0.6. The product of these

values (7.2E-5/yr) represents a bounding relay room fire scenario delta core

damage frequency (CDF) for this finding. Since the bounding result is consistent

with the licensees conclusion, the SRA determined that the delta core damage

frequency for the finding was less than 1E-4/yr, which is less than Red.

42

In addition, the licensee entered this issue into their corrective action program

as CAP 01475242. As a result, the inspectors concluded that the violation met

all four criteria established by Section 9.1(a) and that the NRC was exercising

enforcement discretion to not cite this violation in accordance with the Interim

Enforcement Policy Regarding Enforcement Discretion for Certain Fire Protection

Issues.

ATTACHMENT: SUPPLEMENTAL INFORMATION

43

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

K. Davison, Site Vice President

T. Conboy, Director of Site Operations

E. Blondin, Engineering Director

W. Paulhardt, Plant Manager

J. Boesch, Maintenance Manager

T. Borgen, Operations Manager

B. Boyer, Radiation Protection Manager

H. Butterworth, Business Support Manager

B. Carberry, Emergency Preparedness Manager

J. Corwin, Security Manager

D. Gauger, Chemistry/Environmental Manager

S. Martin, Performance Assessment Manager

M. Pearson, Regulatory Affairs Manager

P. Wildenborg, Sr. Health Physicist

S. Redner, Project Manager, Engineering Programs

P. Brunsgaard, Manager, Engineering Programs

T. Downing, ISI Engineering

J. Wren, NDE Level III

G. Carlson, Senior Licensing Engineer, Regulatory Affairs

E. Baker, Chemist

J. Callahan, Fleet EP Manager

P. Oleson, Regulatory Analyst

U.S. Nuclear Regulatory Commission

K. Riemer, Chief, Reactor Projects Branch 2

T. Beltz, Project Manager, Office of Nuclear Reactor Regulation

Attachment

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000306/2015004-01 NCV Failure to Meet ANSI N14.6 Section 5.3.1 Requirements

(Section 1R08.1)05000282/2014005-02 NCV Failure to Adequately Calibrate Liquid Effluent Monitors

(Section 2RS5.1)

Closed

05000306/2015004-01 NCV Failure to Meet ANSI N14.6 Section 5.3.1 Requirements

(Section 1R08.1)05000282/2014005-02 NCV Failure to Adequately Calibrate Liquid Effluent Monitors

(Section 2RS5.1)05000282/2014002-00 LER Diesel Generators Declared Inoperable Due to Not

Meeting High Energy Line Break Requirements

(Section 4OA3.2)05000282/2014002-01 LER Diesel Generators Declared Inoperable Due to Not

Meeting High Energy Line Break Requirements

(Section 4OA3.2)05000282/2015001-00 LER Fan Coil Unit Leak (Section 4OA3.3)05000282/2015002-00 LER Fan Coil Unit Leak (Lower Head) (Section 4OA3.4)05000282/2015003-00 LER Unanalyzed Condition Due to Non-Compliance with

10 CFR 50 Appendix R (Section 4OA3.5)

Discussed

None.

2

LIST OF DOCUMENTS REVIEWED

The following is a partial list of documents reviewed during the inspection. Inclusion on this list

does not imply that the NRC inspector reviewed the documents in their entirety, but rather that

selected sections or portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

1R04 Equipment Alignment (71111.04)

- 1C28.1 AOP4; Restarting Unit 1 AFWP After Low Suction/Discharge Pressure Trip; Revision 6

- CAP 01002789; AF System Components with Incorrect Quality Level; November 3, 2005

- CAP 01271632; MRB-028 AF System Components are Incorrect Quality Level;

February 18, 2011

- C28-2; Auxiliary Feedwater System Unit 1; Revision 52

- CAP 01500181; QF1142 in WO-472499 Needs More Info; November 4, 2015

- Condition Report Search from January 1, 2010 to October 1, 2015

- DBD SYS-28B; Prairie Island Nuclear Generating Plant Design Bases Document; Revision 8

- Drawing B-15300; Min. Flow Orifice Assembly; August 27, 1970

- Drawing NF-39222; Feedwater & Aux Feedwater Unit 1; Revision 83

- Letter from Pacific Pumps Dresser to Northern States Power Company; Minimum

Flow-Nuclear Service Pumps Comments to NRC Bulletin 88-04; September 16, 1988

- Letter from U.S. NRC Office of Material Safety and Safeguards; NRC Regulatory Issue

Summary 2015-06 Tornado Missile Protection; June 10, 2015

- SE-0302 Equipment Details; Valve AF-26-5; 11 TD AFW PMP Oil Clr Outl to Sump

- SE-0302 Equipment Details; Valve AF-33-1; 11 TD AFW PMP Recirc to 11 CST

- SWI Eng-30 Addendum-A; Prairie Island Nuclear Generating Plant Q-List Downgrade

Resolution Project Position Papers; Revision 1

- Temporary Change Request 084A for SP 1100 12; Motor Driven AFW Pump Monthly Test;

Revision 84

- USAR Appendix I; Prairie Island Updated Safety Analysis Report; Revision 33

- CAP 01500373; Question by NRC in Regards to Drawings in SharePoint; November 5, 2015

- CAP 01500324; Safety Function for RCP Inlet and Outlet MVs Evaluation; November 5, 2015

- SP 2251; Caustic Addition Valve Quarterly Test; Revision 13

- H5; Motor Operated Valve Program; Revision 19

- H10.1.B; Inservice Testing Program Component Basis Document; Revision 3

- CAP 01502434; 21 Caustic Standpipe Level Spiked Low to Low Alarm Set-point;

November 18, 2015

- DBD SYS-8D; Containment Spray System Design Basis Document; Revision 4

- B18D; Containment Spray System Bases Document; Revision 9

- NF-39252; Caustic Addition System Unit 1 & 2 Flow Diagram; Revision 83

- B18D; Containment Spray System Description; Revision 9

1R05 Fire Protection (71111.05)

- NF-39228-1; Fire Protection and Screen Wash System Unit 1 & 2 Flow Diagram; Revision 91

- F5 Appendix A; Fire Area 71 Requirements; Revision 13

- F5 Appendix F; Fire Hazards Analysis Matrix; Revision 30

- NF-39228-3; Sprinkler Fire Protection System Turbine U 2-Screen-house Unit 1 & 2;

Revision 78

3

- CAP 01504212; Unexpected FP Annunciator in Unit 2 Feedwater Pump Area;

December 1, 2015

- CAP 01504521; NRC Question: Fire Strategies Shows Containment Fire Extinguishers;

December 3, 2015

1R06 Flooding (71111.06)

- 1C28.1 AOP2; Loss of Condensate Supply to Aux Feed Water Pump Suction; Revision 0

- 5AWI 8.9.0; Internal Flooding Drainage Control; Revision 15

- C31 AOP1; Fire Protection Line Break; Revision 3

- Calculation 1067-0022-001; Determination of Flow Path Input for Floor Drains; Revision 0

- Calculation ENG-ME-586; Effects of Flooding in the AFW Pump Room from a Postulated

Pipe Rupture; June 9, 2005

- Calculation ENG-ME-759; Gothic Internal Flooding Calculation for the Turbine Building;

Revision 1D

- Drawing NF-38213; Turbine Room-Concrete Plan of Base Slab Floor Drains-Class I Area;

Revision G

- H36; Plant Flooding; Revision 10

- TP 1398; Verify Physical Inputs to Internal Flooding Evaluations; Revision 5

- WO 00501079-01; TP 1398-Internal Flooding Input Verifications/Evals Eng:

TP 1398-(Non-RCA Areas) Internal Flooding Input Evals; May 5, 2015

1R07 Annual Heat Sink Performance (71111.07A)

- WO 498516-01; 22 CC HX South Internal Inspection; Revision 0

1R08 Inservice Inspection Activities (71111.08)

- Safety Evaluation Related to the Control of Heavy Loads; Dated 06/06/83

- ANSI N14.6; American National Standards for Special Lifting Devices for Shipping Containers

Weighing 10 000 Pounds or More for Nuclear Materials; 1978 Edition

- Calculation ENG-CS-361; Evaluation of the Acceptability of the Reactor Vessel Head Lift Rig,

Reactor Vessel Internals Lift Rig, Load Cell and Linkage to the Requirements of NUREG 0612;

Revision 0

- NDE Report Nos. BOP-MT-15-040-051,021-023; Magnetic Particle Examination of Reactor

Vessel Internals Lift Fixture Welds; Dated 10/27/15

- WO 00457321; Perform NDE Magnetic Particle Examination of Reactor Head Lifting Rig;

Dated 10/23/15

- NDE Report No. 2005M008; Magnetic Particle Examination of Reactor Head Lift Fixture;

Dated 06/03/05

- WO 457197-07; Perform NDE Exams of Reactor Vessel Internals Lifting Device;

Dated 10/24/15

- CAP 01457469; Operating Experience (IN 2014-02) Item Evaluated: Crane and Heavy Lift

Issues Identified; Dated 01/12/15

- Engineering Evaluation EC 26341; Reactor Vessel Internal Lift Rig Torque Tube Weld

Evaluation; Dated 10/26/15

- WO 00436724; SP 1392 Unit 1 RCS System Bolting Inspection; Dated 08/05/14

- CAP 01450417; BACC Evaluation for ISI Indication on CV-31325; Dated 10/11/14

- CAP 01450480; BACC Evaluation for ISI Indication on RC-19-1; Dated 10/11/14

- CAP 01450476; BACC Evaluation for ISI Indication on 135-011; Dated 10/11/4

- CAP 01427328; BACC Evaluation for Leak Identified in Unit 2 Containment 21 Vault;

Dated 04/17/14

4

- CAP 01498446; Functionality Assessment of Reactor Vessel Internals Lifting Device;

Dated 10/29/15

- CAP 01412727; Leak From Capped Drain Downstream of 2RC-8-19; Dated 12/30/13

- CAP 01431405; Boric Acid Leak was Found on 2RC-8-31; Dated 05/20/14

- CAP 01469111; Boric Acid Packing Leak on 2SI-35-6; Dated 03/06/15

- CAP 01492989; Boric Acid Built Up Below 21 SI Pump; Dated 09/11/15

- CAP 01445383; 22 Safety Injection Pump IB/OB Mechanical Seal Leakage; Dated 09/04/14

- WO 00406128; Remove and Replace Valve 2RC-7-2, Loop A to Pressurizer CV 31228

BY-PASS; Dated 09/28/13

- H2; Boric Acid Corrosion Control Program; Revision 25

- NDE Report No. 2015V011; VT-3 of AFWH-79 Sway Strut/Clamp; Dated 10/21/15

- FP-PE-NDE-530; Visual Examination, VT-3; Revision 8

- CAP 01499213; Internals Lift Rig Question; Dated 10/29/15

- CAP 01497779; NRC Question in Regards to ISI Exam of Reactor Head Lift Rig; Dated

10/21/15

- CAP 01497774; PM 3560-52 Needs to be Revised for Better Work Execution; Dated 10/21/15

- PM 3560-52; Reactor Head Lifting Rig Spreader & Connection Legs Assembly Inspections;

Revision 13

- CAP 01452946; ISI Indication on Hanger 1RSIH-415; Dated 10/25/14

- CAP 01414257; Non-Conformance with ASME Section XI; Dated 01/13/14

- CAP 01429434; Potential ISI Issue for ANII Procedure Reviews; Dated 05/05/14

- CAP 01452105; Metallic Item Found on the Reactor Vessel Flange; Dated 10/20/14

- NDE Report No. 2015U023; Ultrasonic Examination of SI Elbow-to-Pipe Weld W-6;

Dated 11/01/15;

- NDE Report No. 2015U044; Ultrasonic Examination of RH Pipe-to-Elbow Weld W-5;

Dated 11/05/15

- NDE Report No. 2015V013; VT-3 of AFWH-64 Sway Strut/Clamp; Dated 10/21/15

- Procedure FP-PE-NDE-402; Ultrasonic Examination of Austenitic Pipe Welds-Supplement 2;

Revision 5

SWI-NDE-ET-1; Bobbin Coil Data Analysis; Revision 6

- SWI-NDE-ET-3; Rotating Coils Data Analysis; Revision 6

- SWI-NDE-ET-6; Array Coil Data Analysis; Revision 1

1R11 Licensed Operator Requalification Program (71111.11)

- 2C1.3-M3; Unit 2 Shutdown to Mode 3; Revision 5

- 2C1.2-M2; Unit 2 Startup to Mode 2; Revision 4

- 2C1.2-M1; Unit 2 Startup to Mode 1; Revision 1

- D30; Post Refueling Startup Testing; Revision 61

1R12 Maintenance Effectiveness (71111.12)

- CAP 01198723; 11 RCP Motor Had High Breakaway Torque Reading; September 21, 2009

- CAP 01490741; IST and MOV Program Discrepancies; August 21, 2015

- WO 532146-16; 21 RCP Seal Replacement; November 30, 2015

- CAP 01500324; Unit 1 and 2 RCP CC Inlet and Outlet MV Operability Evaluation; November

6, 2015

- CAP 01250606; HELB Interaction in Aux Building Overstress CC Piping; September 21, 2010

- NF-39216-1; Cooling Water-Screen-house Unit 1 & 2; Revision 89

- EC 13000; High Energy Line Break Evaluation for Component Cooling Water Piping in the

Turbine Bldg; Revision 0

5

1R13 Maintenance Risk Assessment and Emergent Work Control (71111.13)

- Shift Manager Logs and Control Room Logs Units 1 & 2; November 17-19, 2015

1R15 Operability Determination and Functional Assessments (71111.15)

- CAP 01504216; AFW Recirc Line Recommended Procedure Change; December 2, 2015

- QF0739; AFWP Recirculation Line Evaluation NRC Response Form; December 2, 2015

- CAP 01500184; AFWP Recirculation Line Seismic Evaluation; November 14, 2015

- CAP 01501764; Additional NRC Question Related to AFW Recirc Line and HELB; November

13, 2015

- NF-39222; Flow Diagram Feedwater and Aux Feedwater Unit 1; Revision 83

- Operating Information 15-63; Auxiliary Feedwater Recirculation Flow Min-flow Requirements;

November 20, 2015

1R19 Post-Maintenance Testing (71111.19)

- H36; Plant Flooding; Revision 10

- CAP 01501977; Six of 97 FCU Pipe Flanges Required Re-torque During PMT; November 16,

2015

- WO 519240-03; Replace SV-33133; October 2, 2015

- CAP 01495575; SV-33133 Stroked Outside Ref. Range During PMT

- CAP 01495499; SV-33133 Failed PMT Testing Under WO 519240; October 2, 2015

- WO 519240-02; SV-33133 Stroke Time Outside Ref. Range; October 2, 2015

- SP 1151A; Train A Cooling Water System Quarterly Test; Revision 20

- CAP 01501698; 21 RCP did not Rotate as Expected During Alignment; November 13, 2015

- WO 492354-06; Mechanical Troubleshooting of 21 RCP; November 17, 2015

1R20 Outage Activities (71111.20)

- CAP 01500324; Safety Function for RCP Inlet and Outlet MVs; November 20, 2015

- Unit Two Refueling Outage October 2015 Shutdown Safety Assessment; Revision 0

- 2C1.4; Unit 2 Power Operation; Revision 56

- 2C1.3-M2; Unit 2 Shutdown to Mode 2; Revision 3

- 2C19.1; Containment Unit 2 Plant Operation Requirements; Revision 23

- CAP 01504150; Identified Issues During Final Unit 2 Containment Walk Through;

December 2, 2015

- CAP 01503211; U2 Rx Vsl Support Fan Motor FLA Question; November 24, 2015

- NF-39220; Unit 1 Condensate System Flow Diagram; Revision 79

- SP 2177; Core Inventory Verification; November 16, 2015

- CAP 01506302; Water Found on 755 Level of U2 CTMT Following Rx Trip;

December 17, 2015

- CAP 01506286; 25B Tube Side Relief Valve Lifted Prior to Taking 22 FWP OOS;

December 17, 2015

- CAP 01504099; Ceiling Leak in Unit 2 Rod Drive Room; December 1, 2015

- CAP 01499287; Leaching was Identified on the 21 RCP Seal Faces; October 29, 2015

- CAP 01499105; MV-32197 as Found Configuration; October 29; 2015

- CAP 01491555; Ball Valve PMs Suspended Due to Parts Unavailability; August 29, 2015

- CAP 01505839; Eddy Current Heating on Unit 2 Generator Bushing Box IPB Duct;

December 14, 2015

6

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)

- Prairie Island Emergency Plan; Revisions 50 and 51

- PINGP-1576; Emergency Action Level Matrix; Revisions 7 and 8

- F3-2.1; Emergency Action Level Technical Bases; Revision 10

- FP-R-EP-02; 10 CFR 50.54(q) Review Process, Revision 11

- QF-0724; 10 CFR 50.54(q) Review Form, Revision 6

- CAP 01506257; NRC ID Wrong Reference Used in 10 CFR 50.54(q) Evaluation; Dated

12/17/15

1EP6 Drill Evaluation (71111.06)

- P9116SE-0101; LOR Cycle 16A Simulator Evaluation; October 1, 2015

2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01)

- RPIP 1331; Radioactive Material Control; Revision 2

- RPIP 1120; Posting of Restricted Areas; Revision 40

- RPIP 1123; Alpha Characterization Smears; Revision 2

- Technical Basis Document;14-001; Alpha Radiation Protection Program; Revision 0

- FP-RP-AM-01; Alpha Monitoring Program; Revision 5

- RPIP 1135; RWP Coverage; Revision 35

- RPIP 1204; Evaluation of Airborne Radioactivity; Revision 20

- RPIP 1202; Gaseous Airborne Radioactive Monitoring; Revision 9

- RPIP 1331; Radioactive Material Control; Revision 2

- RPIP 1300; Control and Tagging of Radioactive Material; Revision 23

2RS2 Occupational ALARA Planning and Controls (71124.02)

- Prairie Island Nuclear Generating Plant 2R28 Radiation Protection Department Outage

Manual; Date Not Provided

- Prairie Island Nuclear Generating Plant; Dose Excellence Plan; 2013-2017; Revision 0

- Prairie Island Nuclear Generating Plant; 2R28 Radiation Protection Department Outage

Report; Steam Generator Project; Dated 02/03/14

- Prairie Island; 1R29 Radiation Protection Department Outage Report; Dated 02/12/15

- FP-RP-SEN-02; Radiological Work Planning and Controls; Revision 3

- RWP and Associated ALARA Files; RWP 152500; 2R29-RTD Replacement Project;

Various Dates

- RWP and Associated ALARA Files; RWP 155021; 10-Year ISI/Corrosion Inspection-2R29;

Various Dates

- RWP and Associated ALARA Files; RWP 152055; Scaffold Standard Work-U2 Outage;

Various Dates

- RWP and Associated ALARA Files; RWP 152300; Primary SG Activities-U2 Outage; Various

Dates

2RS5 Radiation Monitoring Instrumentation (71124.05)

- CAP 01490581; Missing Documents for Radiation Monitor Primary Calibrations;

August 20, 2015

- CAP 01494632; Cal of Process Rad Monitors Dose Meet H4 ODCM Standard;

September 25, 2015

- CAP 01500149; Additional Eff Rad Monitors Require Evaluation; November 4, 2015

7

- Offsite Dose Calculation Manual (ODCM); Revision 29

- 1R19; Unit 1 Steam Generator Blowdown Monitor Calibration; August 25, 2010

- 2R19; Unit 2 Steam Generator Blowdown Monitor Calibration; April 7, 1993

- 2R19; Unit 2 Steam Generator Blowdown Monitor Calibration; October 15, 2015

- R-18; Waste Effluent Liquid Monitor Calibration; April 7, 1993

- R-18; Waste Effluent Liquid Monitor Calibration; October 2, 2015

4OA1 Performance Indicator Verification (71151)

- FP-R-PI-01; Preparation of NRC Performance Indicators; Revision 3

- FP-R-PI-01; Preparation of NRC Performance Indicators; Attachment 6; RCS Specific

Activity; Various Dates

- FP-R-PI-01; Preparation of NRC Performance Indicators; Attachment 9; Occupational

Exposure Control Effectiveness; Various Dates

- FP-R-PI-01; Preparation of NRC Performance Indicators; Attachment 10; RETS/ODCM

Radiological Effluent Occurrence; Various Dates

4OA2 Identification and Resolution of Problems (71152)

- C37.9; Control, Relay, and Computer Room Ventilation; Revision 28

- C37.14; Service Building Ventilation System; Revision 13

- CAP 01469452; NRC Questioned Relative Humidity Level in Multiple Areas; March 10, 2015

- CAP 01468498; NRC Identified-Question CR Humidity Requirements; March 3, 2015

- CAP 01447443; Computer Room Low Humidity; September 21, 2014

- CAP 01498739; C37.14 Rev. 13 (Secondary); November 17, 2015

- CAP 01276040; GL-08-01 TI-177 Drawing Error on NF-39252; March 18, 2011

- PI-21.3B.002; Namco Limit Switch Series Qualification H, K; Revision 1

- EC 00026393; Relative Humidity Impact(s) on Electrical Components; Revision 0

- CAP 01495083; ERCS Alarm for Low Humidity; September 29, 2015

- CAP 01494719; Control Room Humidifiers Should be Repaired or Abandoned;

September 25, 2015

- CAP 01495292; C37.9, Revision 28, Relay, and Computer Room Ventilation; October 1, 2015

- WO 531436; ERCS Alarm for Low Humidity; October 1, 2015

- CAP 01501381; 31 Namco Position Switches are Past Qualified Life; November 11, 2015

4OA3 Follow-Up of Events and Notices of Enforcements Discretion (71153)

- CAP 01506299; NUE HU2.1 Declared Following Fire Alarm in U2 CTMT; December 17, 2015

- CAP 01506281; Flakes Found on U2 CTMT A/S Particle Filter; December 17, 2015

- CAP 01506285; Unit 2 Reactor Trip Due to Turbine Trip; December 17, 2015

8

LIST OF ACRONYMS USED

ADAMS Agencywide Document Access Management System

AFW Auxiliary Feed Water

ALARA As-Low-As-Is-Reasonably-Achievable

ANSI American National Standards Institute

ASME American Society of Mechanical Engineers

BWR Boiling Water Reactor

BACC Boric Acid Corrosion Control

CAP Corrective Action Program

CC Component Cooling

CDF Core Damage Frequency

CFR Code of Federal Regulations

CL Cooling Water

DC direct current

EAL Emergency Action Level

EC Engineering Change

ECCS Emergency Core Cooling System

EDG Emergency Diesel Generator

EPRI Electric Power Research Institute

ERCS Emergency Response Computer System

ET Eddy Current

FCU Fan Cooling Unit

HELB High Energy Line Break

IMC Inspection Manual Chapter

INPO Institute of Nuclear Power Operations

IN Information Notice

IP Inspection Procedure

IPEEE Individual Plant Examination of External Events

IR Inspection Report

ISI Inservice Inspection

LER Licensee Event Report

MSPI Mitigating Systems Performance Index

NCV Non-Cited Violation

NDE Nondestructive Examination

NEI Nuclear Energy Institute

NFPA National Fire Protection Association

NIST National Institute of Standards and Technology

NRC U.S. Nuclear Regulatory Commission

ODCM Offsite Dose Calculation Manual

OSP Outage Safety Plan

PARS Publicly Available Records System

PD Performance Deficiency

PI Performance Indicator

PM Planned or Preventative Maintenance

PWR Pressurized Water Reactor

RCA Radiologically Controlled Area

RCP Reactor Cooling Pump

RCS Reactor Coolant System

RETS Radiological Effluent Technical Specifications

RFO Refueling Outage

9

RTD Resistance Temperature Detector

RWP Radiation Work Permit

SER Safety Evaluation Report

SDP Significance Determination Process

SG Steam Generator

SI Safety Injection

SRA Senior Risk Analyst

SSC Structures, Systems, Components

TB Turbine Building

TS Technical Specifications

USAR Updated Safety Analysis Report

VT-3 Visual Examination

WO Work Order 10

K. Davison -2-

In accordance with Title 10 of the Code of Federal Regulations (CFR) 2.390, Public

Inspections, Exemptions, Requests for Withholding, of the NRC's "Rules of Practice," a copy of

this letter, its enclosure, and your response (if any) will be available electronically for public

inspection in the NRCs Public Document Room or from the Publicly Available Records

System (PARS) component of the NRC's Agencywide Documents Access and Management

System (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Kenneth Riemer

Branch 2

Division of Reactor Projects

Docket Nos. 50-282; 50-306;72-010

License Nos. DPR-42; DPR-60; SNM-2506

Enclosure:

IR 05000282/2015004; 05000306/2015004

cc: Distribution via LISTSERV

DISTRIBUTION:

Kimyata MorganButler Carole Ariano

RidsNrrPMPrairieIsland Resource Linda Linn

RidsNrrDorlLpl3-1 Resource DRPIII

RidsNrrDirsIrib Resource DRSIII

Cynthia Pederson Jim Clay

Darrell Roberts Carmen Olteanu

Richard Skokowski ROPreports.Resource@nrc.gov

Allan Barker

ADAMS Accession Number: ML16039A364

Publicly Available Non-Publicly Available Sensitive Non-Sensitive

OFFICE RIII RIII RIII RIII

NAME KRiemer/bw

DATE 02/08/2016

OFFICIAL RECORD COPY