ML22222A173

From kanterella
Jump to navigation Jump to search
Integrated Inspection Report 05000282/2022002 and 05000306/2022002
ML22222A173
Person / Time
Site: Prairie Island  Xcel Energy icon.png
Issue date: 08/11/2022
From: Hironori Peterson
Region 3 Branch 3
To: Domingos C
Northern States Power Company, Minnesota
References
IR 2022002
Download: ML22222A173 (21)


See also: IR 05000282/2022002

Text

Mr. Christopher P. Domingos

Site Vice President

Prairie Island Nuclear Generating Plant

Northern States Power Company, Minnesota

1717 Wakonade Drive East

Welch, MN 55089-9642

SUBJECT:

PRAIRIE ISLAND NUCLEAR GENERATING PLANT - INTEGRATED

INSPECTION REPORT 05000282/2022002 AND 05000306/2022002

Dear Mr. Domingos:

On June 30, 2022, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at

Prairie Island Nuclear Generating Plant. On July 22, 2022, the NRC inspectors discussed the

results of this inspection with you and other members of your staff. The results of this

inspection are documented in the enclosed report.

One finding of very low safety significance (Green) is documented in this report. This finding

involved a violation of NRC requirements. We are treating this violation as a non-cited violation

(NCV) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violation or the significance or severity of the violation documented in this

inspection report, you should provide a response within 30 days of the date of this inspection

report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,

ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional

Administrator, Region III; the Director, Office of Enforcement; and the NRC Resident Inspector

at Prairie Island Nuclear Generating Plant.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; and the

NRC Resident Inspector at Prairie Island Nuclear Generating Plant.

August 11, 2022

C. Domingos

2

This letter, its enclosure, and your response (if any) will be made available for public inspection

and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document

Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public

Inspections, Exemptions, Requests for Withholding.

Sincerely,

Hironori Peterson, Chief

Branch 3

Division of Reactor Projects

Docket Nos. 05000282 and 05000306

License Nos. DPR-42 and DPR-60

Enclosure:

As stated

cc w/ encl: Distribution via LISTSERV

Signed by Peterson, Hironori

on 08/11/22

ML22222A173

SUNSI Review

Non-Sensitive

Sensitive

Publicly Available

Non-Publicly Available

OFFICE

RIII

RIII

NAME

NShah:sw

HPeterson

DATE

08/11/2022

08/11/2022

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

Inspection Report

Docket Numbers:

05000282 and 05000306

License Numbers:

DPR-42 and DPR-60

Report Numbers:

05000282/2022002 and 05000306/2022002

Enterprise Identifier:

I-2022-002-0054

Licensee:

Northern States Power Company

Facility:

Prairie Island Nuclear Generating Plant

Location:

Welch, Minnesota

Inspection Dates:

April 01, 2022, to June 30, 2022

Inspectors:

S. Bell, Health Physicist

K. Pusateri, Resident Inspector

D. Tesar, Senior Resident Inspector

Approved By:

Hironori Peterson, Chief

Branch 3

Division of Reactor Projects

2

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees

performance by conducting an integrated inspection at Prairie Island Nuclear Generating Plant,

in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the

NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer

to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to Complete Required Inservice Testing Prior to Restoring Equipment to Operation

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Mitigating

Systems

Green

NCV 05000282,05000306/2022002-01

Open/Closed

[H.14] -

Conservative

Bias

71111.15

The inspectors identified a Green finding and associated non-cited violation of Title 10 of the

Code of Federal Regulations (10 CFR) Part 50.55a, "Codes and Standards" for the failure to

meet the inservice testing requirements set forth in the American Society of Mechanical

Engineers (ASME) Operations and Maintenance (O&M) Code and Addenda for failure to

complete required testing prior to returning equipment to operation following maintenance on

the 22 diesel driven cooling water pump (DDCLP).

Additional Tracking Items

None.

3

PLANT STATUS

Unit 1 operated at or near rated thermal power for the entire inspection period.

Unit 2 operated at or near rated thermal power for the entire inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. The inspectors performed activities described in IMC 2515,

Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of

IPs. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel to assess licensee performance and compliance with Commission rules

and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

External Flooding Sample (IP Section 03.03) (1 Sample)

(1)

The inspectors evaluated that flood protection barriers, mitigation plans, procedures,

and equipment are consistent with the licensees design requirements and risk

analysis assumptions for coping with external flooding on May 3, 2022.

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following

systems/trains:

(1)

Unit 1 B train safety injection system on April 22, 2022

(2)

122 control room ventilation returned to service on May 26, 2022

(3)

instrument air system walkdown on May 26, 2022

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a

walkdown and performing a review to verify program compliance, equipment functionality,

material condition, and operational readiness of the following fire areas:

(1)

Fire Zone 43, bus 111 and 121 switchgear rooms on April 4, 2022

(2)

Fire Zone 19, Unit 1 auxiliary building, elevation 715' on April 7, 2022

4

(3)

Fire Zone 26, bus 112 and train A event monitoring rooms, elevation 735' on

April 22, 2022

(4)

Fire Zone 96, transformer 2RX on May 3, 2022

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01)

(1 Sample)

(1)

Observed licensed operator requalification scenarios on May 3, 2022

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (7 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the

following planned and emergent work activities to ensure configuration changes and

appropriate work controls were addressed:

(1)

2RY transformer work on April 25, 2022

(2)

12 electro-hydraulic oil pump leak (potential Initiating Event) on May 2, 2022

(3)

Unit 2 turbine oil cooler 2CL-27-4 on April 25, 2022

(4)

SP 2857, "4kV Bus 21/22 Undervoltage and Underfrequency Relay Test (Omicron),"

on May 24, 2022

(5)

12 CFCU inoperability not MRFF on May 5, 2022

(6)

Work Week 2219 SI pump risk on May 10, 2022

(7)

CAP 501000063397 11, "Condensate Storage Tank Leaking," on May 27, 2022

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (6 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the

following operability determinations and functionality assessments:

(1)

SP 2284, "CV-31733 Closing Time Outside of REF," on April 13, 2022

(2)

AR 501000062700, "122 Control Room Air Handler," on May 2, 2022

(3)

12 CFCU unplanned inoperability on May 5, 2022

(4)

Work Order 700097233, "D5 Ruskin Damper Positioner Replacement," on

June 6, 2022

(5)

22 DDCLP comprehensive test not performed on April 5, 2022

(6)

D5 rack differential detector CAP 501000064219

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02)

(2 Samples)

The inspectors evaluated the following temporary or permanent modifications:

5

(1)

122 safeguards traveling screen T-MOD on May 11, 2022

(2)

11 condensate storage tank leak repairs on May 27, 2022

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (7 Samples)

The inspectors evaluated the following post-maintenance testing activities to verify system

operability and/or functionality:

(1)

Post-maintenance testing (PMT) of MV-32033 on April 28, 2022

(2)

11 charging pump PMT on May 25, 2022

(3)

PMT of circuit breaker 112E-2 on June 1, 2022

(4)

WO 700097233, "D5 Ruskin Damper Positioner Replacement," on June 6, 2022

(5)

22 charging pump PMT on June 8, 2022

(6)

22 CC pump work window and PMT on June 29, 2022

(7)

SP 2089B, "RHR Pump and Suction Valve Quarterly Test," on June 20, 2022

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance testing activities to verify system operability

and/or functionality:

Surveillance Tests (other) (IP Section 03.01) (5 Samples)

(1)

SP 1110B, "Train B Cooling Water Header Isolation Valves Quarterly Test," on

April 28, 2022

(2)

SP 2334, "D5 Emergency Diesel Generator 24 Hour Load Test," on May 1, 2022

(3)

SP 2295, "D5 Diesel Generator 6-Month Fast Start Test," on May 1, 2022

(4)

SP 2088A, "21 SI Pump Quarterly Test," on May 10, 2022

(5)

SP 2307, "D6 DG 6 Month Fast Start Test," on May 23, 2022

Inservice Testing (IP Section 03.01) (1 Sample)

(1)

SP 2857, "4kV Bus 21/22 Undervoltage and Underfrequency Relay Test (Omicron),"

on May 26, 2022

Containment Isolation Valve Testing (IP Section 03.01)

SP 2284, "RCDT Vent Header Containment Isolation Valves Quarterly Test," on

April 13, 2022

6

RADIATION SAFETY

71124.01 - Radiological Hazard Assessment and Exposure Controls

Radiological Hazard Assessment (IP Section 03.01) (1 Partial)

(1)

(Partial)

The inspectors evaluated how the licensee identifies the magnitude and extent of

alpha radiation levels and the concentrations and quantities of radioactive materials

and how the licensee assesses radiological hazards.

71124.03 - In-Plant Airborne Radioactivity Control and Mitigation

Permanent Ventilation Systems (IP Section 03.01) (1 Sample)

The inspectors evaluated the configuration of the following permanently installed ventilation

systems:

(1)

Radioactive waste building ventilation system

Temporary Ventilation Systems (IP Section 03.02) (1 Sample)

The inspectors evaluated the configuration of the following temporary ventilation systems:

(1)

Temporary HEPA ventilation system on the decontamination booth 695' auxiliary

building

Use of Respiratory Protection Devices (IP Section 03.03) (1 Sample)

(1)

The inspectors evaluated the licensees use of respiratory protection devices.

Self-Contained Breathing Apparatus for Emergency Use (IP Section 03.04) (1 Sample)

(1)

The inspectors evaluated the licensees use and maintenance of self-contained

breathing apparatuses.

71124.04 - Occupational Dose Assessment

Source Term Characterization (IP Section 03.01) (1 Sample)

(1)

The inspectors evaluated licensee performance as it pertains to radioactive source

term characterization.

External Dosimetry (IP Section 03.02) (1 Sample)

(1)

The inspectors evaluated how the licensee processes, stores, and uses external

dosimetry.

Internal Dosimetry (IP Section 03.03) (2 Samples)

The inspectors evaluated the following internal dose assessments:

7

(1)

Two internal dose assessments dated October 19, 2021

(2)

One internal dose assessment dated April 23, 2020

Special Dosimetric Situations (IP Section 03.04) (3 Samples)

The inspectors evaluated the following special dosimetric situations:

(1)

Declared pregnant worker records dated April 1, 2020

(2)

Declared pregnant worker records dated March 5, 2020

(3)

Declared pregnant worker records dated September 23, 2021

71124.06 - Radioactive Gaseous and Liquid Effluent Treatment

Walkdowns and Observations (IP Section 03.01) (4 Samples)

The inspectors evaluated the following radioactive effluent systems during walkdowns:

(1)

Turbine building sump effluent compositor and associated sampling lines

(2)

1R19 and 2R19 steam generator blowdown effluent monitors and sample lines

(3)

1R18 liquid waste discharge monitor and associated sample lines

(4)

Unit 1 auxiliary building ventilation system including the 1R30 and 1R37

effluent monitors

71124.07 - Radiological Environmental Monitoring Program

Environmental Monitoring Equipment and Sampling (IP Section 03.01) (1 Sample)

(1)

The inspectors evaluated environmental monitoring equipment and observed

collection of environmental samples (air samples, water samples and TLD locations).

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

BI02: RCS Leak Rate Sample (IP Section 02.11) (1 Sample)

(1)

Unit 1 (April 1, 2021, through March 31, 2022)

Unit 2 (April 1, 2021, through March 31, 2022)

71152A - Annual Follow-up Problem Identification and Resolution

Annual Follow-up of Selected Issues (Section 03.03) (1 Sample)

The inspectors reviewed the licensees implementation of its corrective action program

related to the following issues:

(1)

The inspectors reviewed the completed corrective actions associated with voids in the

residual heat removal (RHR) system in the Mitigating Systems Cornerstone. The

8

inspectors determined if the corrective actions had been completed as documented in

the CAP.

71152S - Semiannual Trend Problem Identification and Resolution

Semiannual Trend Review (Section 03.02) (1 Sample)

(1)

The inspectors reviewed the licensees CAP for potential adverse trends in

Operability Determinations that might be indicative of a more significant safety issue.

INSPECTION RESULTS

Failure to Complete Required Inservice Testing Prior to Restoring Equipment to Operation

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Mitigating

Systems

Green

NCV 05000282,05000306/2022002-01

Open/Closed

[H.14] -

Conservative

Bias

71111.15

The inspectors identified a Green finding and associated non-cited violation of Title 10 of the

Code of Federal Regulations (10 CFR) Part 50.55a, "Codes and Standards" for the failure to

meet the inservice testing requirements set forth in the American Society of Mechanical

Engineers (ASME) Operations and Maintenance (O&M) Code and Addenda for failure to

complete required testing prior to returning equipment to operation following maintenance on

the 22 diesel driven cooling water pump (DDCLP).

Description:

On Saturday, March 26, 2022, the licensee performed routine maintenance on the

22 DDCLP. Upon completion of the maintenance, the licensee performed post maintenance

testing (PMT) as specified in the work order (WO) by completing the quarterly portion of

SP 1106B, "22 Diesel Cooling Water Pump Monthly Test," [performed at 9000 gpm] and

declared the 22 DDCLP as operable.

On Monday, March 28, 2022, the Inservice Testing (IST) Engineer initiated

CAP 501000061742, "Comp Not Performed After 22 DDCLP Maint," which identified the

following:

1) During the maintenance, the pump was uncoupled [diesel engine uncoupled from right

angle drive] as well as other minor maintenance activities.

2) Per the ASME OM Code Subsection ISTB-3310, "Effect of Pump Replacement, Repair,

and Maintenance on Reference Values," "When a reference value or set of values may have

been affected by repair, replacement, or routine servicing of a pump, a new reference value

or set of values shall be determined in accordance with ISTB-3300, or the previous value

reconfirmed by a comprehensive or Group A test run before declaring the pump operable."

3) IST [group] was also not given a review of the WO prior to maintenance.

Subsequently, station personnel reviewed the CAP initiated by the IST Engineer and made

the determination through their Operability process to return the DDCLP to operation based

upon the data obtained from the quarterly surveillance test performed as the PMT on

March 26, 2022.

9

The inspectors, on March 29, questioned whether it was appropriate to return the DDCLP to

service, given that there was a reasonable potential for the reference values to have changed

due to the maintenance performed. Therefore, the conservative action should have been to

verify the applicable reference values for the pump prior to returning it to service.

Title 10 CFR 50.55(a)(1)(iv) incorporates by reference the ASME Operation and Maintenance

Code (O&M Code). O&M Code subsection ISTB-3000 "General Testing Requirements,"

specifies the inservice testing requirements which are to be completed in accordance with

(IAW) Table ISTB-3000-1. The IST required data applicable to the 22 DDCLP per

Table ISTB-3000-1 are, differential pressure, flow rate, and vibration measurements.

ISTB-3540, "Vibration" - ISTB-3540(b) specifies further requirements in that, "Vibration

measurements shall be taken on the upper motor bearing housing in three approximately

orthogonal directions, one of which is the axial direction."

By letter L-PI-14-015 dated April 09, 2014, Prairie Island Nuclear Generating Plant (PINGP)

submitted Relief Request RR-03 seeking relief from code requirement ISTB-3540(b) which

required that vibration measurements be taken on the upper motor-bearing housing in three

approximately orthogonal directions, one of which must be in the axial direction. In lieu of this

code requirement, PINGP proposed as an alternative to take vibration measurements on the

right-angle drive in three orthogonal directions, one of which being in the axial direction, as

well as one additional vibration measurement to be taken on each of the diesel engines. The

NRC approved this relief request by response dated December 5, 2014 (ML14329A185).

As indicated in the CAP, ISTB-3310, "Effects of Pump Replacement, Repair, and

Maintenance on Reference Values," requires that:

ISTB-3312, "When a reference value or set of reference values may have been affected by

repair or routine maintenance, other than that covered under ISTB-3311, the following shall

be performed before declaring the pump operable:

(a) A group A or comprehensive test shall be performed and

(1) the previous reference values reconfirmed or

(2) a new reference value, or set of reference values, shall be determined in accordance

with ISTB-3300."

The Inspectors identified that because the diesel engine and right-angle drive were

uncoupled and re-coupled during the maintenance, and that each of these components are

locations for IST vibration data collection, that the potential existed that "a reference value or

set of reference values may have been affected" by the maintenance activity. One of the

purposes of performing the comprehensive test is to ensure that no unintended flaws or

consequences were introduced during the performance of the maintenance. Therefore, the

inspectors determined that the requirements of ISTB-3312(a)(1) (Subsection ISTB-3310)

would apply to this maintenance activity, and a comprehensive test was required to have

been performed prior to restoring the pump to operation.

In addition, licensee procedure H10.1 "ASME Inservice Testing Program" Section 5.6,

"Establishing a New Reference Value for Pump Testing", quotes ASME OM Code, ISTB-3310

"When a reference value or set of values may have been affected by repair, replacement, or

routine servicing of a pump, a new reference value or set of values shall be determined in

accordance with ISTB-3300, or the previous value reconfirmed by a comprehensive or Group

A test run before declaring the pump operable." Step 5.6.4 further requires that "The

10

minimum USAR flow required for accident mitigation [10,400 gpm] shall be the limiting

acceptance criteria for operability. If the flow is less than the USAR requirement, then the

pump shall be declared inoperable, and the appropriate LCO condition entered."

Subsequently, on Wednesday March 31, 2022, the licensee took actions to perform the IST

comprehensive pump test per the applicable portions of SP 1106B, "22 Diesel Cooling Water

Pump Monthly Test." The results of this test indicated that the vibration data was like what

was seen prior to the maintenance.

Corrective Actions: CAP 501000061742, "Comp Not Performed After 22 DDCLP Maint"

Performance Assessment:

Performance Deficiency: The licensee's failure to perform inservice testing IAW regulatory

requirements in 10 CFR 50.55a, O&M Code Section 3310, and in accordance with their

prescribed procedure (H10.1, "Inservice Testing") prior to returning the equipment to

operation was a Performance Deficiency.

Screening: The inspectors determined the performance deficiency was more than minor

because it was associated with the Equipment Performance attribute of the Mitigating

Systems cornerstone and adversely affected the cornerstone objective to ensure the

availability, reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences. The inspectors reviewed Inspection Manual Chapter 0612

App E, "Examples of Minor Issues", and determined that this issue was most closely related

to example 2.b. Specifically, the Licensee failed to complete the required in-service testing

prior to returning the equipment to operation.

Significance: The inspectors assessed the significance of the finding using IMC 0609

Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The

violation was determined to be of very low safety significance and screened to Green

because inspectors answered all screening questions as "no". Although the DDCLP was

inoperable based on failure to perform the comprehensive inservice testing, the subsequent

performance of the test resulted in pump data like pre-maintenance and therefore the risk

associated with pump operation and functionality resulted in very low risk. This was also in

part due to crediting the 121-motor driven cooling water pump as being available from a

Probabilistic Risk Analysis perspective.

Cross-Cutting Aspect: H.14 - Conservative Bias: Individuals use decision making-practices

that emphasize prudent choices over those that are simply allowable. A proposed action is

determined to be safe to proceed, rather than unsafe in order to stop. The licensee failed to

use conservative decision-making following initiation of a CAP which identified that the O&M

Code required performance of the comprehensive test prior to restoring the equipment to

operable status. The licensee only performed the quarterly surveillance test to return the

pump to operation. Following the CAP initiation, the licensee incorrectly declared the

equipment operable and considered it available to perform its specified safety function.

Enforcement:

Violation: Title 10 CFR 50.55(a)(1)(iv) requires, in part, "When a reference value or set of

values may have been affected by repair, replacement, or routine servicing of a pump, a new

reference value or set of values shall be determined in accordance with ISTB-3300, or the

previous value reconfirmed by a comprehensive or Group A test run before declaring the

11

pump operable."

Contrary to the above, on March 28, 2022, the licensee returned the 22 DDCLP to operation

following maintenance without completing the comprehensive pump test run.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with

Section 2.3.2 of the Enforcement Policy.

Observation: Annual Review of Residual Heat Removal Voids Found After 2R32

Refueling Outage

71152A

Inspectors selected Unit 2 residual heat removal (RHR) voiding long term actions for this

annual follow-up sample to evaluate the timely disposition of this operability issue and ensure

that corrective actions are commensurate with the safety significance. Inspectors reviewed

the corrective action program (CAP) documents associated with a series of voids found

following the 2R32 refueling outage. The significance of the voids was that in some cases

the size of particular voids found exceeded the operability limits listed in procedure H64, Gas

Accumulation Management Program. The licensee was able to perform Operability

Evaluations to determine that the voids were acceptable to maintain reasonable assurance

of Operability.

The licensee determined this potential gaseous intrusion mechanism was related to chemical

additions to the RHR system while it was aligned in Shutdown Cooling Mode.

The licensee created actions in the CAP to revise procedures to minimize the amount of gas

left in the system following Shutdown Cooling Mode. The licensee created corrective actions

to perform more void inspections during subsequent outages and to have engineering ensure

both RHR pumps operate prior to plant heat-up after an outage.

Inspectors noted that corrective actions associated with changing the fill and vent procedures

following an outage were closed to the procedure change requests (PCRs) but then those

PCRs were subsequently cancelled. The licensee as part of their normal review process,

plans to review the PCRs and add justification for the cancellation.

Since all actions are not completed and the licensee has not gone through another refueling

outage, the inspectors cannot yet assess the adequacy and effectiveness of all the corrective

actions.

The licensee-initiated CAP 501000064413 which created a tracking action for completion of

the PCRs. The CAP has not been closed by the licensee so there is an opportunity to assess

the effectiveness of all the corrective actions prior to the next RFO and CAP closure.

No findings or violations were identified during the review.

Observation: Trend Review of ASME O&M Code Compliance

71152S

Inspectors reviewed Operability determinations associated with ASME Code compliance for

trending. Two examples were identified for evaluation as follows:

On October 27, 2021, CAP 501000057742, "SP 2269 Performed UNSAT," was initiated by

the licensee to document the failure of 2SI-6-4 to pass its in-service testing acceptance

criteria. The station performed an Operability Determination (CAP 501000057644,

12

500000316013) and concluded that "Valve 2SI-6-4 is not fully qualified. This is due to not

meeting the leakage criteria established per the IST Code. This condition does not affect the

ability of 2SI-6-4 to perform its specified safety functions...," the licensee concluded that

2SI-6-4 was "Operable."

On October 28, 2021, CAP 501000057820, "Operability Process and Regulatory

Requirements," was initiated by the licensee (and related to CAP 501000057742) to

document in part, that the fleet procedure FP-OP-OL-01 for Operability was updated to

incorporate guidance from NEI 18-03, "Operability Determination." The guidance was not

endorsed by the NRC. The CAP also documented that "the regulatory aspect of how

compliance with 10 CFR 50.55a is maintained still needs to be addressed."

As documented in Inspection Report 2021-004, the NRC identified "... a green finding and

associated non-cited violation of Title 10 of the Code of Federal Regulations (10 CFR)

Part 50.55a(f)(4) for the failure to meet the in-service testing requirements set forth in the

American Society of Mechanical Engineers (ASME) Operations and Maintenance Code and

Addenda after Check Valve 2SI-6-4 exceeded its ASME Code leakage acceptance criteria..."

On March 28, 2022, CAP 501000061742, "Comp Not Performed After 22 DDCLP

Maintenance," was initiated to document the failure to perform the comprehensive test on the

22 diesel driven cooling water pump (DDCLP) following maintenance in accordance with the

ASME operation and maintenance (O&M) Code requirements.

As documented in this inspection report (2022-002), the NRC identified "... a green finding

and associated non-cited violation of Title 10 of the Code of Federal Regulations (10 CFR)

Part 50.55a, "Codes and Standards" for the failure to meet the in-service testing requirements

set forth in the American Society of Mechanical Engineers (ASME) Operations and

Maintenance (O&M) Code and Addenda for failure to complete required testing prior to

returning equipment to operation following maintenance on the 22 diesel driven cooling water

pump (DDCLP)."

On June 20, 2022, CAP 501000064047, "2SI-6-4 and FP-OP-OL-01," was initiated. This

CAP identified that during the 2022 in-service testing focused self-assessment, "It was

identified that there is currently no procedure guidance in FP-OP-OL-01 or other actions in

place to prevent recurrence." (Allowing the plant to move forward in power ascension without

following the ASME OM Code)

The inspectors reviewed the above issues and identified differences in the Xcel Energy Fleet

Procedure FP-OP-OL-01, "Operability" and NRC Inspection Manual Chapter 0326

"Operability Determinations" with respect to code compliance and operability. Subsequently,

the Licensee initiated fleet CAP 501000065231, "NRC insight on IMC-0326 v FP-OP-OL-01."

Inspectors reviewed the CAPs and actions listed above and determined that at the time of

review, there were no actions in place to address the differences between licensee

procedures, NRC Inspection Manuals, and compliance with 10 CFR 50.55a Code

Requirements. CAP 501000057820 had an action to provide training which was documented

as complete in January of 2022; however, this action does not appear to have been effective

based upon the events which occurred on March 28, 2022. CAP 501000064047 was initiated

after the inspectors had started their trend review, and this CAP does capture the

observations of the inspectors. Actions being implemented in this CAP may resolve the

identified gaps, however, since the actions had not yet been created, inspectors were unable

to assess their overall adequacy.

13

No new findings or violations were identified during this trend review.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On July 22, 2022, the inspectors presented the integrated inspection results to

Mr. C. Domingos, Site Vice President, and other members of the licensee staff.

On June 22, 2022, the inspectors presented the radiation protection baseline inspection

results to Mr. S. Skoyen, Acting Plant Manager, and other members of the licensee staff.

14

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

CY-ENVR-003

Three Day Flood Forecast Reporting

6

Procedures

SP 1293

Inspection of Flood Control Measures

27

71111.01

Work Orders

WO 700083238-

0010

SP 1293 Annual Inspection of Flood Contr

06/02/2022

Calculations

M-385-FP-001

Analysis of Record and Engineering Calculations for Cardox

Piping Equivalent Length

2

Drawings

NF-39244

Flow Diagram Instrument Air Piping Unit 1 & 2

98

71111.04

Procedures

C1.1.35-3

Checklist for Cooling Water System

45

F5 Appendix A

Fire Detection Zone 26, Bus 112 & Train A Event Monitoring

Rooms El. 735'

46

F5 Appendix A

Fire Detection Zone 43

46

F5 Appendix A

Fire Detection Zone 19

46

Fire Plans

F5 Appendix A

Fire Detection Zone 96 Transformer 2RX

46

NFPA No. 12-

1972

Standard of Carbon Dioxide Extinguishing Systems

1972

71111.05

Miscellaneous

QF0739, NRC

Question

Response, CAP

501000063724

Pertaining to ENG-ME-804 CO2, Concentration in the Relay

and Cable Spreading Room Attachment 10.1 Retrotec Final

Report Cardox Validation Project

0

Engineering

Changes

EC

601000003804

11 CST: Temp Clamp for Thru-Wall Leak

0

Procedures

SP 2857

4KYV Bus 21/22 Undervoltage and Underfrequency Relay

West (Omicron)

1

71111.13

Work Orders

WO 700106197-

0010

Replace O-Rings/Seals on Flex Hose Fittings

05/01/2022

Calibration

Records

ENG-ME-804

CO2 Concentration in the Relay Room and Cable Spreading

Room

0

Corrective Action

Documents

AR

501000061742

Comp not Performed after 22 DDCLP Maint

03/29/2022

71111.15

Engineering

Changes

EC

602000018704

Revise SP 1091 Monthly Containment Fan Coils Units

Surveillance Test

05/06/2022

71111.15

Miscellaneous

API Standard 650

Welded Steel Tanks for Oil Storage

September

15

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

2003

API Standard 653

Tank Inspection, Repair, Alternation, and Reconstruction

September

2003

C1.1.19-4

Containment and Shield Building Penetration Checklist - Unit

2

53

H10.1

ASME Inservice Testing Program

42

H10.1.B

Inservice Testing Program Component Basis Document

6

OMN-16

ASME Code Case OMN-16 - Use of a Pump Curve for

Testing

2

QF0739, NRC

Question

Response Form

Requested API 650 and API 653

06/02/2022

Operability

Evaluations

CV-31733 / SP

2284 / WO 700099357

IST 96 Hour Evaluation

04/13/2022

FP-OP-OL-01

Operability

22

SP 2284

RCDT Vent Header Containment Isolation Valves Quarterly

Test

20

Procedures

TP 1806

122 Control Room Chiller Inspection

18

Drawing NF-

39220

Flow Diagram Condensate System Unit 1

82

71111.18

Drawings

Drawing XH-74-

56

General Plan 30-29 High Dome Roof

76

GMP GREE-001

CVCS Suction Stabilizer Maintenance

6

GMP SULL-001

SULLAIR Station Air Compressor 1000 Hour Preventative

Maintenance

9

Procedures

PE MCC-G7

MCC Electrical Preventive Maintenance for GE 7700 Line

MCCS

44

WO 700025194

PE-121C-16 BKR PM, 2TB LP B CL HDR MV-320

04/28/2022

WO 700089255

245-042 SPD Reducer Oil Chang Smpl

06/08/2022

WO 700093503

22 CHG PMP CVCS SUCT STABLZR MAINT

03/19/2022

WO 700096494

PMT 125 STA AIR COMPR 1000 HR PM

05/25/2022

WO 700096494

GMP SULL-001-125 STA AIR CMPR 1000 HR PM

05/28/2022

71111.19

Work Orders

WO 700096614

MD-32421 Insp. and Adjust Ruskin SR MD

05/28/2022

16

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

WO 700097233

21 D5 DSL RM OA (MD-32420) RPLC POSNR

06/07/2022

WO 700097663

MD-32422 Insp & Adjust Ruskin SR M

06/16/2022

WO 700097663

MD-32422 Insp &n Adjust Ruskin SR M

06/16/2022

SP 1110B

Train B Turbine Cooling Water Header Isolation Valves

Quarterly Test

7

SP 2088A

Train A Safety Injection Quarterly Test

37

SP 2284

RCDT Vent Header Containment Isolation Valves Quarterly

Test

20

SP 2295

D5 Diesel Generator 6 Month Fast Start Test

57

SP 2307

D6 Diesel Generator 6 Month Fast Start Test

51

SP 2334

D5 Diesel Generator 24 Hour Load Test

24

Procedures

SP 2857

4kV Bus 21/22 Undervoltage and Underfrequency Relay

Test (Omicron)

1

WO 700092735

SP2334 - D5 DG 24 Hour Load Test

03/04/2022

WO 700095690

SP 111OB TRN B CL HDR ISOL VLVS TEST

04/28/2022

WO 700096197

SP 2857 Bus 21/22 Undervolt Omicron

05/23/2022

WO 700097314

SP2295 D5 DG 6MO Fast Start Test

05/01/2022

WO 700099357

SP2284 RCDT VENT HDR CTMT ISOL VLVS QTR

04/12/2022

WO 700099357

SP 2284 RCDT Vent HDR CTMT Isolation Valves Qtr

03/23/2022

71111.22

Work Orders

WO 700105218

SP2307 D6 DG Fast Start Test

05/23/2022

Corrective Action

Documents

Resulting from

Inspection

AR

501000062752

Alpha Analysis

05/03/2022

Engineering

Evaluations

Prairie Island Plant Alpha Characterization Study

11/26/2021

71124.01

Radiation

Surveys

2R32 Refueling Outage Radiation Surveys

Various

ALARA Plans

2R32 Refuel Work Radiation Protection Job Plan

09/28/2021

Four Quantitative Respirator Mask Fit Tests

05/02/2022

71124.03

Miscellaneous

Respiratory Protection Qualification Records for Day Shift

Reactor Operators and Senior Reactor Operators for May 4,

2022.

Various

17

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Annual SCBA Tests for units LAD090896 and LAD090890

07/13/2021

43525-0

Breathing Air Tests December 2021

12/09/2021

Miscellaneous

4433895-0 and

433653-1

Breathing Air Checks for November 2021

11/15/2021

FP-RP-RPP-02

Respirator Fit Testing and Portacount Fit Tester Operation

1

Procedures

RPIP 1604

Breathing Air Test

17

Self-Assessments

Inspection Procedure 71124.03

Undated

71124.03

Work Orders

7000680170020

12 Shield Building Ventilation Filter Removal Efficiency Test

08/18/2020

AR

501000047700

Improper Area TLD Changeout

01/23/2021

Corrective Action

Documents

AR

501000050416

Dose Discrepancies for Period 2, 2020

04/16/2021

17-005

Technical Basis Document Passive Monitoring Capability

Testing

11/05/2019

SSA

606000001052

2019 Prairie Island Isotopic Mix Evaluation

Undated

Engineering

Evaluations

SSA

606000001454

2021 Prairie Island Isotopic Mix Evaluation

Undated

Three Declared Pregnant Worker Records

Various

2021 Annual Area TLD Trending

02/21/2022

Period 2 (July - December) 2021 Dosimetry Data

Undated

Mirion Technologies Inc., Oak Ridge TN, NVLAP

Accreditation for 07/01/2021 through 06/30/2022

Miscellaneous

Period 2 (July through December 2021). 2021 Dose

Discrepancy Reports

Various

FP-RP-DR-01

Dosimetry Program

15

Procedures

FP-RP-IDA-01

Internal Dose Assessment

4

71124.04

Radiation Work

Permits (RWPs)

220059

Dose Restricted Individuals

0

H4

Offsite Dose Calculation Manual

32

71124.07

Procedures

RPIP 4721

REMP Air Sampling

22

71152A

Miscellaneous

602000018696

Adverse Condition Monitoring Plan for Unit 2 RHR Discharge

Voids

01/06/2022

18

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Operability

Evaluations

POD

50100000316297

Prompt Operability Determination for Unit 2 Train A RHR

Piping

0