IR 05000282/2024001

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Reissued Integrated Inspection Report 05000282/2024001 & 05000306/2024001
ML24346A370
Person / Time
Site: Prairie Island  Xcel Energy icon.png
Issue date: 01/13/2025
From: Richard Skokowski
NRC/RGN-III/DORS/RPB3
To: Conboy T
Northern States Power Company, Minnesota
References
IR 2024001
Download: ML24346A370 (1)


Text

SUBJECT:

PRAIRIE ISLAND NUCLEAR GENERATING PLANT - REISSUED INTEGRATED INSPECTION REPORT 05000282/2024001 AND 05000306/2024001

Dear Thomas Conboy:

The U.S. Nuclear Regulatory Commission (NRC) identified two internal process errors in NRC INTEGRATED INSPECTION REPORT 05000282/2024001 AND 05000306/2024001, dated May 15, 2024 (ADAMS Accession No. ML24135A177). Both errors occurred in the Inspection Results Section, Failure to Provide Adequate Oversight to Supplementary Personnel Resulting in a Reactor Trip.

First, Unit 2 was incorrectly assessed the same as Unit 1, using Inspection Manual Chapter (IMC) 0609 Appendix A, The Significance Determination Process (SDP) for Findings At-Power. Based on Unit 2 being shut down for a refueling outage at the time of the event, the proper significance classification for the Unit 2 finding was minor, consistent with the IMC 0612 Appendix B, Issue Screening.

Second, Unit 1, although IMC 0609 Appendix A, The Significance Determination Process (SDP) for Findings At-Power, was the correct Appendix, subsequent review of the issue determined that the event warranted a detailed risk evaluation (DRE), instead of being screened to GREEN as was originally documented. Specifically, using IMC 0609 Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Exhibit 1-Initating Events Screening Questions, under B, Transient Initiators, the inspectors should have determined the finding required a detailed risk evaluation because the finding caused both a reactor trip and the loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition (e.g., loss of condenser). As a result, a DRE was completed consistent with our process. The conclusion of the DRE was that the finding for Unit 1 remained GREEN, and the results of the DRE are documented in the revised inspection report.

As a result of errors, the NRC has reissued the report in its entirety to correct these errors.

January 13, 2025 This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Richard A. Skokowski, Chief Reactor Projects Branch 3 Division of Operating Reactor Safety Docket Nos. 05000282 and 05000306 License Nos. DPR-42 and DPR-60

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000282 and 05000306

License Numbers:

DPR-42 and DPR-60

Report Numbers:

05000282/2024001 and 05000306/2024001

Enterprise Identifier:

I-2024-001-0078

Licensee:

Northern States Power Company

Facility:

Prairie Island Nuclear Generating Plant

Location:

Welch, MN

Inspection Dates:

January 01, 2024 to March 30, 2024

Inspectors:

M. Abuhamdan, Reactor Inspector

T. Ospino, Resident Inspector

K. Pusateri, Resident Inspector

D. Tesar, Senior Resident Inspector

Approved By:

Richard A. Skokowski, Chief

Reactor Projects Branch 3

Division of Operating Reactor Safety

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Prairie Island Nuclear Generating Plant, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to Adequately Implement the Requirements of 10 CFR 50, Appendix B, Criterion XVI Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000282,05000306/2024001-01 Open/Closed

[P.3] -

Resolution 71111.20 The inspectors identified a Green finding and associated non-cited violation of Title 10 of the Code of Federal Regulations (10 CFR), Part 50, Appendix B, Criterion XVI, Corrective Action, associated with the licensees failure to correct conditions adverse to quality (CAQ).

Specifically, the inspectors identified that the licensee failed to take adequate corrective actions to correct a CAQ. Consequently, this failure would have allowed a CAQ associated with safety related structures, systems, and components (SSCs) to remain uncorrected absent inspector intervention.

Failure to Provide Adequate Oversight to Supplementary Personnel Resulting in a Reactor Trip Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events Green FIN 05000282,05000306/2024001-02 Open/Closed

[H.2] - Field Presence 71153 The inspectors identified a Green finding when the licensee failed to meet the standards of procedure FP-MA-COM-02, Oversight and Control of Supplementary Personnel.

Specifically, the licensee failed to provide supplemental workers with an appropriate level of oversight and engagement to ensure performance was commensurate with station standards, resulting in a loss of all non-safeguards busses and a Unit 1 turbine and reactor trip.

Additional Tracking Items

Type Issue Number Title Report Section Status URI 05000306/2024001-01 Unresolved Item Associated with Modifications to Motor-Operated Valve Limit Switch 71111.18 Closed LER 05000282,05000306/2023

-001-01 LER 2023-001-01 for Prairie Island Nuclear Generating Plant, Units 1 and 2, Reactor Trip, Auxiliary Feedwater and Emergency Service Water 71153 Closed

System Actuation due to Electrical Transient in DC Control Power Cables LER 05000282,05000306/2023

-001-00 LER 2023-001-00 for Prairie Island Nuclear Generating Plant, Units 1 and 2, Reactor Trip, Auxiliary Feedwater and Emergency Service Water System Actuation due to Electrical Transient in DC Control Power Cables 71153 Closed

PLANT STATUS

Unit 1 entered the inspection period shut down in Mode 3 (hot standby). Unit 1 went critical on January 24, 2024, entered Mode 1 (power operation) on January 27, 2024, and reached full-rated thermal power on January 29, 2024. Unit 1 was then shut down to Mode 3 to facilitate repairs on a main feed pump discharge line on February 8, 2024. Unit 1 returned to critical on February 11, 2024, entered Mode 1 on February 12, 2024, and reached full-rated thermal power on February 14, 2024. Unit 1 maintained at or near full-rated thermal power for the remainder of the inspection period.

Unit 2 entered the inspection period shut down for refueling outage 2R33. Unit 2 went critical on February 29, 2024, reached Mode 1 on March 1, 2024, and reached 50 percent power on March 2, 2024. Unit 2 subsequently tripped from 50 percent power and entered Mode 3 on March 3, 2024. Unit 2 returned to critical on March 7, 2024, Mode 1 on March 8, 2024, and reached full-rated thermal power on March 18, 2024. Unit 2 remained at or near full-rated thermal power for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Seasonal Extreme Weather Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated readiness for seasonal extreme weather conditions prior to the onset of a winter storm for the following systems:

AB-2 entry for winter storm warning on January 11, 2024

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) D6 emergency diesel generator on January 3, 2024
(2) C1.1.38 common fuel system status on January 4, 2024
(3) D1/D2 diesel generators on March 11, 2024
(4) Unit 2 auxiliary feedwater system on March 13, 2024

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1)door 43 fire impairment and fire areas 8 and 32 on February 20, 2024 (2)fire zone 82, D1 diesel room on March 11, 2024 (3)fire zone 35, battery rooms 21 and 22 on March 13, 2024 (4)fire zone 2, auxiliary feed pump room, elevation 695' on March 13, 2024 (5)fire zone 1, battery rooms 11 and 12 on March 13, 2024

Fire Brigade Drill Performance Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated the onsite fire brigade training and performance during an unannounced fire drill for crew five on March 19, 2024.

71111.06 - Flood Protection Measures

Flooding Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated internal flooding mitigation protections following failure of door 43 to close on February 28, 2024.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (7 Samples)

(1) The inspectors observed and evaluated licensed operator performance in the control room during Unit 1 reactor startup on January 24, 2024.
(2) The inspectors observed and evaluated licensed operator performance in the control room during Unit 1 reactor shutdown for a steam leak on February 8, 2024.
(3) The inspectors observed and evaluated licensed operator performance in the control room during Unit 1 reactor startup from a forced outage on February 11, 2024.
(4) The inspectors observed and evaluated licensed operator performance in the control room during Unit 2 reactor startup from a refueling outage with source range NI failure on February 20, 2024.
(5) The inspectors observed and evaluated licensed operator performance in the control room during Unit 2 reactor startup from a refueling outage on February 29, 2024.
(6) The inspectors observed and evaluated licensed operator performance in the control room during Unit 2 trip response on March 3, 2024.
(7) The inspectors observed and evaluated licensed operator performance in the control room during Unit 2 reactor startup from a forced outage on March 7, 2024.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated licensed operator requalification training as-found testing on March 18, 2024.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (6 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:

(1)21 cooling water pump replacement on January 17, 2024 (2)multiple trips CB401 breaker on 28 inverter on January 17, 2024

(3) Corrective Action Plan (CAP) 501000079768, ISI [inservice inspection] Indication Evaluation for SP2168.13, on January 17, 2024
(4) MV-32019 21 turbine-driven auxiliary feedwater (TDAFW) pump steam inlet isolation valve on January 18, 2024
(5) Work Order (WO) 700087060, 22 TDAFW Pump Maintenance, on February 22, 2024 (6)condensate demineralizer review following Unit 2 reactor trip on March 4, 2024

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (6 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1)operational decision-making instruction (ODMI) for Unit 1 startup on January 8, 2024 (2)risk evaluation for transition from shutdown risk to online risk on January 15, 2024 (3)risk associated with emergent issues on Unit 1 circulating water and impact on Unit 1 startup on January 18, 2024 (4)extended operation in lowered inventory risk evaluation on February 6, 2024

(5) ODMI & adverse condition monitoring plan for Unit 2 startup with 22 reactor coolant pump (RCP) second seal degraded on February 29, 2024 (6)risk management following Unit 2 trip and subsequent startup on March 4, 2024

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (8 Samples)

The inspectors evaluated the licensees justifications and actions associated with the following operability determinations and functionality assessments:

(1)reactor coolant system evaluation for Technical Specification 3.4.3 on October 25, 2023 (2)source range nuclear instrument seismic qualification on December 5, 2023

(3) CAP 501000080389, "D6 Fuel Oil Leak Getting Worse," on January 3, 2024 (4)past operability review MV-32019 21 TDAWF pump on January 11, 2024 (5)application of Technical Specification Limiting Condition for Operation (LCO) 3.0.4.b for mode change on January 25, 2024 (6)bus 25/26 and bus 27 circuit breaker sequencing on February 6, 2024 (7)prompt operability determination for D1/D2 HELP question on February 29, 2024
(8) CAP 501000082220, "POD 50000327699 Unit 1 HELB," on March 6, 2024

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated refueling outage activities from January 1, 2024, to March 1, 2024.

71111.24 - Testing and Maintenance of Equipment Important to Risk

The inspectors evaluated the following testing and maintenance activities to verify system operability and/or functionality:

Post-Maintenance Testing (PMT) (IP Section 03.01) (8 Samples)

(1) WO 700133040, CV-31321 Diaphragm Leaking (PMT/LLRT [local leak rate test]),

on January 11, 2024 (2)22 reactor coolant pump seal replacement PMT on January 17, 2024 (3)22 turbine driven auxiliary feedwater pump PMT on January 31, 2024

(4) WO 700087060, 22 Turbine Driven AFW [auxiliary feedwater] Pump Quarterly Test - PMT," on February 18, 2024
(5) WO 700127367, MV-32016, on March 13, 2024
(6) WO 700135613, SP 2406 MSIV [main steam isolation valve] In Service Test, on March 21, 2024
(7) SP 1073B, Monthly Train B Shield Building Ventilation System Test, on March 25, 2024
(8) WO 700133173, SP 1106B 22 DDCL [diesel-driven cooling water] Pump Comprehensive Test, on March 25, 2024

Surveillance Testing (IP Section 03.01) (4 Samples)

(1) WO 700044983, SP 1070 Rx Coolant Sys Integrity Test, on January 11, 2024
(2) SP 2750, Containment Close-out, on January 29, 2024
(3) SP 2750, Containment Close-out, on February 16, 2024
(4) WO 700125323, SP 1155B 12 Component Cooling Water Quarterly Surveillance, on March 20, 2024

Inservice Testing (IST) (IP Section 03.01) (1 Sample)

(1) WO 700125737, SP 1106C 121 Cooling Water Pump Quarterly Test, on February 22, 2024

Reactor Coolant System Leakage Detection Testing (IP Section 03.01) (2 Samples)

(1) LLRT total leak rate for Unit 2 2R33 refueling outage on October 6, 2023
(2) SP 2070, RCS Integrity Test Unit 2, on January 1,

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:

IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01)===

(1) Unit 1 (January 1, 2023, through December 31, 2023)
(2) Unit 2 (January 1, 2023, through December 31, 2023)

IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02) (2 Samples)

(1) Unit 1 (January 1, 2023, through December 31, 2023)
(2) Unit 2 (January 1, 2023, through December 31, 2023)

IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 02.03) (2 Samples)

(1) Unit 1 (January 1, 2023, through December 31, 2023)
(2) Unit 2 (January 1, 2023, through December 31, 2023)

MS09: Residual Heat Removal Systems (IP Section 02.08) (2 Samples)

(1) Unit 1 (January 1, 2023, through December 31, 2023)
(2) Unit 2 (January 1, 2023, through December 31, 2023)

71153 - Follow Up of Events and Notices of Enforcement Discretion Event Follow up (IP Section 03.01)

(1) The inspectors evaluated site response to the Unit 1 trip on January 25, 2024.

Event Report (IP Section 03.02) (2 Samples)

The inspectors evaluated the following licensee event reports (LERs):

(1) LER 05000282, 05000306/2023-001-00 for Prairie Island Nuclear Generating Plant, Units 1 and 2, Reactor Trip, Auxiliary Feedwater and Emergency Service Water System Actuation due to Electrical Transient in DC Control Power Cables (ADAMS Accession No. ML23338A277). The inspection conclusions associated with this LER are documented in this report under Inspection Results Section 71153. This LER is closed.
(2) LER 05000282, 05000306/2023-001-01 for Prairie Island Nuclear Generating Plant, Units 1 and 2, Reactor Trip, Auxiliary Feedwater and Emergency Service Water System Actuation due to Electrical Transient in DC Control Power Cables (ADAMS Accession No. ML24081A153). The inspectors reviewed the updated LER submittal.

The previous LER submittal was also reviewed in this inspection report under Inspection Results Section 71153. This LER is closed.

INSPECTION RESULTS

Unresolved Item (Open)

Unresolved Item Associated with Modifications to Motor-Operated Valve Limit Switch URI 05000306/2024001-01 71111.18

Description:

During the 2R33 refueling outage, modifications were made to the safety related limit switch installed on motor-operated valve, MV-32019, 21 steam generator main steam supply to the 22 turbine-driven auxiliary feedwater pump. Specifically, the gears inside the replacement switch were stainless steel rather than bronze (not like for like), the intermittent shaft had an additional hole drilled through it perpendicular to the manufacturer provided hole, and the orientation of the rotor was changed from that provided by the vendor.

Planned Closure Actions: Review licensee evaluation of the changes in material and the modifications made to the limit switch, their impact on seismic qualification, and the potential impact to operability.

Licensee Actions: Evaluate the impact of the differences in material and the impact of the modifications made as well as the resultant impact on seismic qualification and potential operability impacts.

Corrective Action References: 501000079553, Bkr 211J-13 Tripped During PMT/RTS 501000079667, Manually Operated MV-32019 per COO-17 501000081027, MOV Limit Switch Grease Related Failures 501000081105, MV-32019 Thermals Tripped D 501000083170, LEGACY: MV-32019 Limit Switch Material 501000083626, MV-32019 Limit Switch Failure to Adequately Implement the Requirements of 10 CFR 50, Appendix B, Criterion XVI Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000282,05000306/2024001-01 Open/Closed

[P.3] - Resolution 71111.20 The inspectors identified a Green finding and associated non-cited violation of Title 10 of the Code of Federal Regulations (10 CFR), Part 50, Appendix B, Criterion XVI, Corrective Action, associated with the licensees failure to correct conditions adverse to quality (CAQ).

Specifically, the inspectors identified that the licensee failed to take adequate corrective actions to correct a CAQ. Consequently, this failure would have allowed a CAQ associated with safety related structures, systems, and components (SSC's) to remain uncorrected absent inspector intervention.

Description:

On February 22, 2024, during the Prairie Island Unit 2 refueling outage, inspectors identified an example where the licensee failed to take corrective actions adequate to resolve the condition adverse to quality absent inspector intervention:

Preventive maintenance (PM) procedure, PM 3132-1-22: 22 TDAFWP [Turbine Driven Auxiliary Feedwater Pump] Minor Insp [Inspection] step 7.10.2 specifies to Measure and Document As-Found data in the corresponding table. The step is followed by the following note: RCE 01132098 indicates that proper coupling alignment is critical in preventing turbine bearing failure. Deviations from the values listed in the Reference table must be evaluated by the System Engineer. The most critical dimension is the vertical offset value due to predicted thermal expansion which would occur during turbine operation. The As-Found data recorded in the table was outside of the values listed in the Reference table in both the horizontal and vertical directions. Despite the note indicating that the values must be evaluated by the system engineer, no CAP was written, and the PM was documented as having been completed satisfactorily. Inspectors determined that this was a condition adverse to quality, and the requisite corrective action to perform an engineering evaluation was not performed, as required by procedure PM 3132-1-22.

Corrective Actions: The licensee has entered the item into the corrective action program and completed the required actions to address the condition adverse to quality.

Corrective Action References: 501000082185

Performance Assessment:

Performance Deficiency: The licensee's failure to identify and correct a condition adverse to quality, such as nonconformances and deficiencies, in accordance with 10 CFR 50, Appendix B, Criterion XVI was a performance deficiency. Specifically, the inspectors identified that during preventive maintenance procedure PM 3132-1-22: 22 TDAFWP Minor Insp, maintenance personnel recorded data which did not meet acceptance criteria, a condition adverse to quality, and the requisite corrective action to perform an engineering evaluation was not performed. Inspectors determined that the failure of the licensee to identify and correct this CAQ was within the ability of the licensee to foresee and correct and was therefore a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Equipment Performance attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Inspectors determined that the licensee's failure to identify and correct a condition adverse to quality could have result in the failure of a safety related SSCs to perform its intended safety function. Specifically, the deviation from acceptance criteria associated with the TDAFWP had the potential to cause premature bearing failure as specified in PM 3132-1-22 and Root Cause Evaluation (RCE) 1132098.

Significance: The inspectors assessed the significance of the finding using IMC 0609 Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors determined that the issue was of very low safety significance and screened to Green by answering "No" to all of the questions in Exhibit 2 - Mitigating Systems Screening Questions.

Cross-Cutting Aspect: P.3 - Resolution: The organization takes effective corrective actions to address issues in a timely manner commensurate with their safety significance. The licensee failed to ensure appropriate corrective actions for a condition adverse to quality were taken in a manner commensurate with its safety significance.

Enforcement:

Violation: The requirements of 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, specifies in part that, "Measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and nonconformances are promptly identified and corrected."

Contrary to the above, from December 5, 2023 thru January 28, 2024, the licensee failed to establish measures to assure that conditions adverse to quality are promptly identified and corrected. Specifically, the licensee failed to identify and correct deviations associated with the as-found acceptance criteria requirements for the Turbine Driven Auxiliary Feedwater Pump (TDAFWP). The as-found turbine bearing coupling alignment data were outside the acceptance criteria values.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Failure to Provide Adequate Oversight to Supplementary Personnel Resulting in a Reactor Trip Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events Green FIN 05000282,05000306/2024001-02 Open/Closed

[H.2] - Field Presence 71153 The inspectors identified a Green finding when the licensee failed to meet the standards of procedure FP-MA-COM-02, Oversight and Control of Supplementary Personnel.

Specifically, the licensee failed to provide supplemental workers with an appropriate level of oversight and engagement to ensure performance was commensurate with station standards, resulting in a loss of all non-safeguards busses and a Unit 1 turbine and reactor trip.

Description:

On October 19, 2023, horizontal directional drilling (HDD) activities were being performed at the Prairie Island Nuclear Generating Plant (PINGP) in support of degraded cable replacement as part of the Unit 2 refueling outage. The HDD was from the plant switchyard to just inside the protected area fence and was being conducted by the Xcel Energy Transmission & Distribution (T&D) group. At 11:10 a.m. on October 19, 2023, with Unit 1 operating at 100 percent power, multiple substation breakers unexpectedly opened and, simultaneously, multiple grounds were detected on direct current (DC) control power cabling from the plant to the substation control house. This resulted in a loss of all non-safety related busses simultaneously with a Unit 1 turbine trip and reactor trip, and the actuation of auxiliary feedwater and emergency service water. Operators responded to the event in accordance with approved plant procedures and safely placed the plant in Mode 3, hot shutdown. NRC inspectors responded to the site to provide oversight of licensee response. Unit 1 was subsequently cooled down to Mode 5, cold shutdown.

The site determined that the HDD in progress at the site damaged DC control cables resulting in the identified plant response. The licensee root cause evaluation determined the root causes were weakness in the excavation permit approval process as well as inadequate oversight of the personnel performing the work. The T&D workers were Xcel Energy employees with authorized access to the respective areas, and little oversight was provided based upon this. However, this was not in compliance with licensee procedure FP-MA-COM-02 Oversight and Control of Supplementary Personnel, Section 2.1, which specifies that oversight be provided to supplemental personnel "anytime work is to be accomplished at NSPM nuclear facilities by personnel other than permanent nuclear business unit employees. The procedure further specifies that it is the responsibility of the department manager/functional area manager or designee to provide in-field oversight, observations, and coaching to supplemental workers.

This finding is NRC-identified because the inspectors had identified a previous weakness in the licensee's oversight of work from the same workgroup (Transmission and Distribution - T&D), both in the quality of work and the oversight of the supplemental workers.

This issue was reviewed using Inspection Procedure 71153, Follow up of Events and Notices of Enforcement Discretion, and was reported in Licensee Event Reports (LERs)05000282, 05000306/2023-001-00 and 05000282, 05000306/2023-001-01 for Prairie Island Nuclear Generating Plant, Units 1 and 2, Reactor Trip, Auxiliary Feedwater and Emergency Service Water System Actuation due to Electrical Transient in DC Control Power Cables (ADAMS Accession Nos. ML23338A277 and ML24081A153).

A Management Directive 8.3 Evaluation Decision Documentation for Reactive Inspection (ML23311A424) was completed and it was determined that the licensees operational performance adequately mitigated the reactor trip event for loss of offsite power to only the non-vital buses and dealt with challenges, and the operators satisfactorily placed the reactor in safe cold shutdown condition. The inspection should continue under the baseline inspection program versus a special inspection (SIT). The basis for the decision is as follows:

  • The equipment degradation was limited to non-safety related equipment. No safety related systems or components were lost during mitigation of the loss of offsite power to the non-vital buses, which limits the overall risk to the issue.
  • The inspectors, due to prompt response to the event and subsequent inspection activities related to the response, have obtained a significant amount of information regarding potential causes of the degraded condition which initiated the event.
  • Licensee performance before, during and after the degradation was identified, and the licensees root cause and corrective actions are being followed by the inspectors.

Corrective Actions: The licensee replaced and tested all damaged cables. In addition, they implemented procedure changes to strengthen the requirements for excavation onsite as well as incorporating duties and responsibilities of individuals responsible for oversight of supplemental personnel.

Corrective Action References: CAP 501000077958

Performance Assessment:

Performance Deficiency: The licensees failure to follow Section 2.1 of procedure FP-MA-COM-02 Oversight and Control of Supplemental Personnel, which requires that oversight be provided to supplemental personnel anytime work is to be accomplished at NSPM nuclear facilities by personnel other than permanent nuclear business unit employee, is a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Human Performance attribute of the Initiating Events cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations.

Unit 1:

Specifically, the horizontal directional drilling led to damage to the DC control power cables, resulting in a loss of all non-safeguards busses, an automatic turbine and reactor trip of Unit 1. The loss of all non-safeguards busses coincident with the turbine and reactor trip of Unit 1 resulted in a "SCRAM with Complications" in accordance with NEI 99-02, revision 7, "Regulatory Assessment Performance Indicator Guideline."

Unit 2:

The inspectors determined the performance deficiency for Unit 2 was minor because failure to comply with licensee procedure FP-MA-COM-02 Oversight and Control of Supplementary Personnel, did not adversely impact the Mitigating Systems and Initiating Events cornerstones due to Unit 2 being in a refueling outage with all nuclear fuel removed from the reactor, and therefore there were no safety consequences.

Significance: The inspectors assessed the significance of the finding using IMC 0609 Appendix A, The Significance Determination Process (SDP) for Findings At-Power. Unit 1:

The inspectors assessed the significance of the finding for Unit 1 using IMC 0609 Appendix A, The Significance Determination Process (SDP) for Findings At-Power. Using IMC 0609, Appendix A, Exhibit 1-Initating Events Screening Questions, under B, Transient Initiators, the inspectors determined the finding required a detailed risk evaluation because the finding caused both a reactor trip and the loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition (e.g., loss of condenser).

A Region III senior reactor analyst (SRA) performed a detailed risk evaluation to assess the significance of the finding. The SRA used SAPHIRE version 8.2.10 and the Prairie Island Standardized Plant Analysis Risk (SPAR) model version 8.82 to determine the significance of the finding. In accordance with the Risk Assessment of Operational Events (RASP)

Handbook, Volume 1, Section 8.4 the SRA performed an initiating event analysis and a condition analysis and determined that the initiating event analysis was the appropriate calculation for this event.

The event was modeled as a loss of condenser heat sink and a failure of non-safeguards busses 11, 13, and 14. The SRA modified the model to reflect the PORV block valves being in the open position, moderator temperature coefficient to account for the time in the operating cycle, and electrical ATWS events to reflect the loss of non-safeguards busses experienced during the event.

The change in core damage frequency (CDF) was estimated to be less than 1E-6/year. The event was modeled as an initiating event and therefore external events were not considered.

The dominant core damage sequence for the event involved a loss of auxiliary feedwater and feed and bleed. The change in large early release frequency (LERF) was also considered and estimated to be below 1E-7/year.

Cross-Cutting Aspect: H.2 - Field Presence: Leaders are commonly seen in the work areas of the plant observing, coaching, and reinforcing standards and expectations. Deviations from standards and expectations are corrected promptly. Senior managers ensure supervisory and management oversight of work activities, including contractors and supplemental personnel.

Specifically, the licensee did not have personnel in the field providing oversight of supplemental workers as specified in Section 2.1 of FP-MA-COM-02 Oversight and Control of Supplementary Personnel.

Enforcement:

Inspectors did not identify a violation of regulatory requirements associated with this finding.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On April 9, 2024, the inspectors presented the integrated inspection results to Thomas Conboy and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

2C1.2-M1

Unit 2 Startup to Mode 1

2C1.2-M2

Unit 2 Startup to Mode 2

C1B

Appendix - Reactor Startup

71111.11Q

Procedures

Fig C1A-3

Estimated Critical Boron Concentration Based on

BEACON-TSM

Prairie Island

Maintenance Rule

Basis Document

Various Functions

Various

Dates

Miscellaneous

SP 2168.13 2R33

CE Boric Acid Indications

71111.12

Procedures

PM 3122-3

Shield Bldg, Category 1 Vent Zone, Fire and Security Door

Inspection

71111.13

Miscellaneous

Extended Operation in Lowered Inventory Operational Fous

Protection Plan

501000080988

Past Operability Review (POR)

2/06/2024

501000081254

Unit 1 Use of LCO 3.0.4

01/24/2024

501000081294

IST Review Mode Change and SP 1155 A/B

01/25/2024

501000081411

SP 2155A Not Complete w/in Periodicity

01/28/2024

501000081422

IST Requirements for Pumps vs 3.0.4

01/29/2024

Corrective Action

Documents

501000081503

AOC - Tech Spec Surveillance SP/ASME/IST

01/30/2024

Engineering

Changes

QF2702, Design

Equivalent

Change,

2000023965

EC 601000004330, Rev. 0, U1 NIS Drawer Replacement

1R34

2/27/2023

Engineering

Evaluations

608000001132

Evaluation of RCS for Continued Operation per Tech. Spec.

3.4.3

LTR-EQ-23-35

Dynamic Similarity Evaluation of NIS Source Range Drawer

Assemblies

2/14/2023

Miscellaneous

LTR-NIS-23-020

Functional Similarity Evaluation of NIS Source Range

Drawer Assemblies

2/14/2023

71111.15

Procedures

MP D27.35

MSIV Closure for Maintenance or Testing

71111.18

Miscellaneous

Limitorque

Technical Update

01-01

Material Color Change

03/05/2001

501000077983

DC Panel Ground

01/10/2024

Corrective Action

Documents

501000078005

DC Panel Ground

01/10/2024

EM 4.3.1-C-6

Connectors

EM 4.3.1-C.7

Electrical Construction Standards Cables

EQ H8-E.1.7.DG

EEQ - SPLICES RAYCHEM INLINE - CRIMP CONN

PLANNERS INSTRUCTIONS

H8-E.1.53.DG

EEQ - Splices EGS Compact Splice Planners Instructions

H8-E.1.8.DG

EEQ - Splices Raychem Inline-Crimp Conn Installers

Instructions

71111.20

Procedures

SP 2072

Local Leakage Rate Test of Containment Penetrations

2M-AF-3132-1-22

Isolation, Restoration and Testing of 22 Aux Feed Pump

D70.12

Motor-Operated Valve Steam Lubrication

MP D65

Auxiliary Feedwater Overspeed TTOD Test

SP 1070

Reactor Coolant System Integrity Test

SP 1073B

Monthly Train B Shield Building Ventilation System Test

SP 1080.2

Shield Building Ventilation Filter Removal Efficiency Test

SP 1106B

Diesel Cooling Water Pump Monthly Test

109

SP 2070

Reactor Coolant System Integrity Test

SP 2070

Reactor Coolant System Integrity Test

Procedures

SP 2406

Main Steam Isolation Valve Inservice Test

WO 700044935

SP 1070 Rx Coolant System Integrity Test

WO 700078684

Troubleshoot Bkr 211J-13 and MV-32019

WO 700087060

PM 3132-1-22: 22 TDAFWP MINOR INSP

09/27/2023

WO 700100220

SP 2070 - Rx Coolant Sys Integrity Tst

WO 700100220

SP 2070 - RX Coolant SYS Integrity Tst

01/28/2024

WO 700119857

CV-31419 Water Leak By

71111.24

Work Orders

WO 700125323

SP 1155B - CC SYS QTR TEST TRN B

WO 700127367

MV-32016 LP A MS to 11 TDAFWP Lube

WO 700133040

Perform As-Found LLRT

WO 700133173

SP 1106B-22 DD CL PMP (245-392) 1 M Test

WO 700133246

Test SI NOT READY Light

WO 700135613

SP 2406 - MSIV Inservice Tst Up from CSD

03/06/2024

Engineering

Evaluations

2000031728

Reactor Trip Report - Unit 2

03/03/2024

QF0431, Rev. 21,

2000031268

Cause Evaluation Template, CAP ID# 501000077958, Unit 1

Reactor Trip

10/19/2023

QF0565, Revision

Maintenance Rule Functional and MSPI Failure Evaluation,

QA# 501000081105

2/01/2023

Miscellaneous

QF1146, Revision

5, Past

Operability

Review

CAP 501000079553

2/01/2023

2C49.5

Placing Unit 2 Condensate Filter Demineralizers on Line

2E-0

Reactor Trip or Safety Injection

C58800

Remote Alarm Response Procedure

OP 2C28.1 AOP4

Restarting Unit 2 AFWP After Low Suction/Discharge

Pressure Trip

71153

Procedures

OP 2C28.2

Unit 2 Feedwater System

46