IR 05000282/2022001

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Integrated Inspection Report 05000282/2022001, 05000306/2022001, and 07200010/2020001
ML22123A140
Person / Time
Site: Prairie Island  Xcel Energy icon.png
Issue date: 05/03/2022
From: Hironori Peterson
Region 3 Branch 3
To: Domingos C
Northern States Power Company, Minnesota
References
IR 2022001
Download: ML22123A140 (17)


Text

SUBJECT:

PRAIRIE ISLAND NUCLEAR GENERATING PLANT - INTEGRATED INSPECTION REPORT 05000282/2022001, 05000306/2022001, AND 07200010/2020001

Dear Mr. Domingos:

On March 31, 2022, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Prairie Island Nuclear Generating Plant. On April 15, 2022, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

No findings or violations of more than minor significance were identified during this inspection.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Branch 3 Division of Reactor Projects Docket Nos. 05000282, 05000306, and 07200010 License Nos. DPR-42, DPR-60, and SNM-2506

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000282, 05000306, and 07200010

License Numbers:

DPR-42, DPR-60, and SNM-2506

Report Numbers:

05000282/2022001, 05000306/2022001, and 07200010/2020001

Enterprise Identifier:

I-2022-001-0068 and I-2021-001-0164

Licensee:

Northern States Power Company

Facility:

Prairie Island Nuclear Generating Plant

Location:

Welch, Minnesota

Inspection Dates:

January 01, 2022, to March 31, 2022

Inspectors:

K. Pusateri, Resident Inspector

D. Tesar, Senior Resident Inspector

Approved By:

Hironori Peterson

Branch 3

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Prairie Island Nuclear Generating Plant, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

None.

PLANT STATUS

Unit 1 began the inspection period at rated thermal power. On March 21, 2022, the unit was down powered to 7 percent for Turbine Control Valve Testing and repairs to the turbine control system. The unit was returned to rated thermal power on March 22, 2022, and remained at or near rated thermal power for the remainder of the inspection period. Unit 2 operated at or near rated thermal power for the entire inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, conducted routine reviews using IP 71152, Problem Identification and Resolution, observed risk significant activities, and completed on-site portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Seasonal Extreme Weather Sample (IP Section 03.01) (1 Sample)

(1) Walkdowns of Exterior Temp Structures, D6 Fuel Oil Vault, CST Warming for Cold Weather on February 1, 2022

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1)21 Motor-Driven Auxiliary Feedwater Pump Post-Surveillance Walkdown on January 6, 2022 (2)21 Battery During D6 Risk Informed Completion Time (RICT) on February 3, 2022 (3)21 and 22 Auxiliary Feedwater Pump Walkdown During D6 (RICT) on January 31, 2022 (4)11 Safety Injection Pump Walkdown on February 16, 2022

(5) Cardox System Walkdown Following Out-of-Service Period on March 4, 2022

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

(1) D1 (A Train) and D2 (B Train) Emergency Diesel Generators (Following Maintenance Window) on February 24, 2022

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (6 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1) Zone 2, Auxiliary Feedwater Pump Rooms, El. 695' on January 6, 2022
(2) Zone 12, Relay and Cable Spreading Room, El. 715' on January 12, 2022
(3) Zone 14, Old P250 Room, El. 715' on January 18, 2022
(4) Zone 17, Access Control, El. 715' on February 24, 2022
(5) Zone 3, 11, and 12 Feedwater Pumps, El 695' on March 10, 2022
(6) Zone 1, Battery Rooms 11 and 12, El 695' on March 9, 2022

Fire Brigade Drill Performance Sample (IP Section 03.02) (1 Sample)

(1) Turbine Building Unit 1, El. 695' on March 14, 2022

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 03.01) Internal Flooding Sample Units 1 and 2 on March 14, 2022

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the Control Room during the Unit 1 Downpower for Turbine Valve Test and 'C' Kernel Replacement on March 23, 2022.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated Licensed Operator Requalification Training (LORT) As-Found Simulator Scenario (DEP) on March 15, 2022.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (2 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:

(1) D6 Unavailability on February 10, 2022
(2) Unit 1 Turbine Stop Valve Testing on March 22, 2022

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (7 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) Contingency Risk Informed Completion Time (RICT) for D6 Work Window Review of Availability Form 4's on January 30, 2022
(2) Phoenix Update for Pressurizer Heater "C" Bank Unavailability on February 22, 2022
(3) WW 2203 D6 Emergency Diesel Generator Maintenance Window on January 18, 2022 (4)22 Reactor Coolant Pump (RCP) Lower Bearing Oil Level Decrease on January 14, 2022 (5)

"B" Cooling Water Return Header Work and RICT Implementation on February 24, 2022

(6) D1 Emergency Diesel Generator Work Window on March 7, 2022 (7)22 Diesel Driven Cooling Water (DDCL) Pump Work Window on March 21, 2022

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (6 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1) Reactor Coolant Pump Casing ASME Code Compliance on January 14, 2022
(2) Door 56 From U2 Side Relay Room to Turbine Building Out-of-Service on February 9, 2022
(3) Fire Protection Change Evaluation 22-002 on March 7, 2022 (4)22 Condensate Pump Offline Predictive Motor Analysis (PDMA) Testing on February 11, 2022
(5) Residual Heat Removal (RHR) System Voids on January 3, 2022 (6)22 DDCL Pump ASME OM Code Non-Compliance on March 29, 2022

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (2 Samples)

The inspectors evaluated the following temporary or permanent modifications:

(1) EC 601000001587 Bypass Computer Room UPS Trip and Halon Automatic Initiation on February 24, 2022
(2) EC 601000003309 Unit 2 Diesel Fuel Oil Storage Tank (FOST) Piping MOD Wax Tape Code Compliance on January 6, 2022

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (6 Samples)

The inspectors evaluated the following post-maintenance testing activities to verify system operability and/or functionality:

(1) WO 700102208-0600 Bypass D6 Magnetic Pickup Unit (MPU) per ECR 601000003587 on February 11, 2022 (2)

"B" Cooling Water Header Return to Service (RTS) Post-Maintenance Testing on February 24, 2022 (3)122 Control Room Cleanup Fan on March 1, 2022

(4) SP 1194 CARDOX (Carbon Dioxide) 18-month System Test as Post-Maintenance Testing on March 4, 2022
(5) WO 700102961-0010 Replace Actuator 1/D6 on February 11, 2022 (6)22 Diesel Driven Cooling Water (DDCL) Pump Post-Maintenance Testing Following Work Window on March 28, 2022

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance testing activities to verify system operability and/or functionality:

Surveillance Tests (other) (IP Section 03.01) (5 Samples)

(1) SP 2095 Bus 26 Load Sequencer on February 1, 2022
(2) SP 2468.1 Unit 2 GL-08-01 Inspections for Modes 1, 3, and 4 on January 18, 2022
(3) SP 1194 CARDOX (Carbon Dioxide) 18-Month System Test on February 17, 2022
(4) SP 2856 Bus 26 Undervoltage Relay Test on February 3, 2022
(5) SP 1054 Turbine Control Valve Testing on March 28, 2022

Inservice Testing (IP Section 03.01) (1 Sample)

(1) SP 2101 21 Motor-Driven Auxiliary Feedwater Pump Quarterly Flow and Valve Test on January 6, 2022

71114.06 - Drill Evaluation

Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01) (1 Sample)

(1) Emergency Preparedness INPO Evaluated Exercise on March 15,

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:

IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01)===

(1) Unit 1 (January 1, 2021, through December 31, 2021) on January 26, 2022
(2) Unit 2 (January 1, 2021, through December 31, 2021) on January 26, 2022 IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02) (2 Samples)
(1) Unit 1 (January 1, 2021, through December 31, 2021) on January 26, 2022
(2) Unit 2 (January 1, 2021, through December 31, 2021) on January 26, 2022

IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 02.03) (2 Samples)

(1) Unit 1 (January 1, 2021, through December 31, 2021) on January 26, 2022
(2) Unit 2 (January 1, 2021, through December 31, 2021) on January 26, 2022

71152A - Annual Follow-up Problem Identification and Resolution Annual Follow-up of Selected Issues (Section 03.03)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) Annual Follow-up of the Solenoid Valve Failure for the D2 Emergency Diesel Generator.

71152S - Semiannual Trend Problem Identification and Resolution Semiannual Trend Review (Section 03.02)

(1) Trend Evaluation for the Quality of Information Provided to NRC on March 16, 2022 71153 - Follow-Up of Events and Notices of Enforcement Discretion Event Follow-up (IP Section 03.01) (2 Partials)

(1)

(Partial)10 CFR 50.9 URI Follow-Up on January 10, 2022 (2)

(Partial)

Follow-Up Violation of T.S. 5.6.6 on January 19,

OTHER ACTIVITIES

- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL 60853 - On-Site Fabrication of Components and Construction on an ISFSI The inspectors evaluated the licensees Independent Spent Fuel Storage Installation (ISFSI)pad expansion activities from February 2021 to January 18, 2022. The expansion and pad design were previously approved by the NRC through a license amendment (ML20237F365). Throughout construction, the inspectors evaluated the following:

Preparation of the subsurface, formwork, and type and condition of reinforcing steel.

The materials used were consistent with the design and procurement specifications.

Aggregates were tested for potential reactivity.

Design changes, modifications, and non-conformance reports.

Qualifications of individuals performing Quality Assurance (QA) functions including non-destructive evaluations.

QA oversight; and

American Concrete Institute (ACI) and American Society for Testing and Materials (ASTM) concrete sample test results, including verifying compressive strength tests met design specifications.

The inspectors were onsite on September 15-16, 2021, and observed the following during construction:

Placement of reinforcing steel was consistent with design requirements.

Concrete placement was consistent with ACI standards.

Concrete testing was consistent with ASTM and ACI standards.

Overall pad dimensions were consistent with the design documents.

INSPECTION RESULTS

Observation: Follow up of D2 Emergency Diesel Generator Solenoid Valve Failure 71152A The Safety-Related (SR), D2 Emergency Diesel Generator (EDG) B air start solenoid valve (SV) failed to change state on August 16, 2021, and was documented in CAP 501000055123, with an action to evaluate the condition and perform an Extent of Condition (EOC) review.

The failed SV was replaced, restoring the system to normal operation on August 19, 2021.

Based upon Operating Experience (OE) data for recent failures of this type of (SV), a CAP action was created for an Engineering Change (EC) to acquire a different SV for installation in 2023. The inspectors also reviewed the procedures and documents from a Part 21 perspective and did not identify any issues with the forensics report which determined that no Part 21 report was required. During the review, inspectors identified that CAP action 500000314662 for the EOC review had been marked as complete, yet it did not include appropriate documentation for action closure. The licensee-initiated CAP 501000062261 to document inadequate closure of the action and to reopen the action for proper completion.

CAP 501000055123 remains open awaiting closure following the EC action completion. The inspectors determined that the actions being taken and/or planned were reasonable and commensurate with the safety significance of the issue. The inspectors did not identify any findings or violations of more than minor significance.

Observation: Semiannual Trend Review of Quality of Documents Provided to the NRC 71152S On September 8, 2021, the inspectors performed a semi-annual trend review regarding a potential adverse trend in the quality of documents being provided to the NRC. These documents were used by the NRC, in part, to evaluate conditions and to determine if, and how much additional inspection is required in specific areas. Inspectors reviewed Corrective Action Program (CAP) items generated in the last year documenting deficiencies with the technical rigor being applied for documents prior to submittal. Some examples of these deficiencies included:

CAP 501000060402 Update NRC response, dated 2/7/2022 Quality Issue Management (QIM) 501000058054 documented that based off H10.1 and H10.1.B the site did not use or implement the SI [Safety Injection] accumulator discharge check valves Check Valve Condition Monitoring (CVCM) plans. The CAP implied that the standard ISTC code requirements were being applied. This information was provided to the NRC on November 5, 2021, via QF0739. However, this information was not fully accurate as CVCM Plans were prepared and signed for the Residual Heat Removal (RHR) cold leg Safety Injection (SI) accumulator discharge check valves to allow for partial flow testing, during the summer of 2019. This was then used as justification to update the surveillance procedures to implement the partial flow testing.

CAP 501000056770 Incorrect information provided to NRC, dated 10/05/2021 This CAP identified that the In-Service Inspection (ISI) Engineer provided information as part of the response to a Request for Information (RFI) for the 2R32 ISI Inspection. However, the information was not fully accurate, in that the response to question B8 SP 2408 was listed as "Containment Power Quarterly Inspection. This was incorrect in two respects, 1) SP 2408 is Walkdown of the Shield Building Annulus and 2) SP 2554 was Containment at Power Quarterly Inspections but was changed to Containment Power Inspection on June 7, 2021.

CAP 501000057560 Rev 8 of PTLR submitted with error, dated 10/21/2021 On September 8, 2021, CAP 501000055874 PTLR 54 EFPY fluence not bounding was issued to document that the fluence values used for developing the Pressure Temperature Limits Report (PTLR) and the associated curves used to limit heat up and cool down, were higher than previously determined.

On October 5, 2021, CAP 501000056729 Fluence Analysis Unexpected High W2 Weld was issued to document an error in the current calculation used to determine fluence values and adjusted reference temperatures (ART). Specifically, the calculation used a wrong dimension for the W2 weld location resulting in fluence values higher than what was previously reported.

As a result, the PTLR heat up and cooldown curves and ARTs needed revision; this also impacted other items that relied on the ARTs and/or PTLR curves as inputs.

On October 8, 2021, Westinghouse provided a letter to Prairie Island Nuclear Generating Plant (PINGP) Impact Assessment for Prairie Island Units 1 and 2 - PTLR Non-Conservatism. This letter identified the calculational error discussed above and determined that the previously calculated fluence values and ARTs at end of life (54 EFPY)and the existing PTLR curves were non-conservative and required revision.

On October 12, 2021, PINGP submitted Revision 8 of the PTLR (previously approved on February 16, 2021) to restore compliance with Technical Specification 5.6.6.C. However, the report referenced the incorrect PTLR curves and apparently had not accounted for the calculational errors discussed in the previous CAPs.

The inspectors reviewed the PINGP Fleet Procedures FP-R-LIC-13, Communications with the NRC, and FP-R-LIC-02, Regulatory Correspondence, which discussed the licensee's requirements and commitments for ensuring that adequate technical rigor was applied prior to submitting information to the NRC. These documents require that reviewers, in part, confirm the following:

Is the information provided complete?

Is the information provided correct? Was the preparer of the response a subject matter expert?

Does the response answer the question being asked? Is the response on topic and clear?

Are inputs and assumptions appropriately validated?

If there is an embedded calculation, is it correct?

If the response contains a condition adverse to quality, was it documented in the CAP?

On January 18, 2022, the Corporate Functional Area Manager (CFAM) of Engineering identified an Area of Concern (AOC) with multiple instances where engineering personnel have provided incorrect information to external stakeholders. An action was developed to stress the What Your Signature Means with Engineering personnel. This action was completed at an Engineering All Hands Meeting in February of 2022, followed by action closure on February 18, 2022. The inspectors review concluded that for the first two examples above where incorrect information was provided to the NRC, the consequences of those were minimal and did not adversely affect the NRCs ability to perform its regulatory function. The third example above is being tracked in the Unresolved Item (URI) documented in Report 2021-004. The licensee implemented corrective actions to assure plant operations are within proper safety limits and have taken actions to correct and update the PTLR and its associated documents. The inspectors have no immediate concerns with the licensees corrective actions; however, based on the relatively short runtime of these actions, the inspectors could not make an assessment regarding their effectiveness for this trend review.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On April 15, 2022, the inspectors presented the integrated inspection results to Mr. C. Domingos, Site Vice President, and other members of the licensee staff.

THIRD PARTY REVIEWS Inspectors reviewed Institute on Nuclear Power Operations reports that were issued during the inspection period.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

501000051919

Concrete Mix Options Not Meet Design Req

05/13/2021

501000053098

Soil Densometer Equipment Deltas

06/11/2021

501000054279

ISFSI Subgrade Compaction Test

07/22/2021

501000054336

Concrete Delivery Rejected at Job Site

07/23/2021

501000054983

NOS: Contractor Uncalibrated M&TE

08/11/2021

501000055049

ISFSI Expansion - Plate Load Test Data

08/13/2021

501000055298

ISFSI Const Subgrade Density Test Missed

08/20/2021

501000059357

ISFSI Expansion - Concrete Pad Thickness

2/30/2021

Westinghouse IR-

21-10020

Near Miss During Concrete Pour at Prairie Island ISFSI

09/16/2021

Westinghouse IR-

21-10068

Water Cement Ratio Exceeded Requirement

09/17/2021

Westinghouse IR-

21-10905

Flatness Inspection of Safety Related Pad

10/06/2021

Westinghouse IR-

21-11816

Pad Flatness at Pullboxes Exceeds Specified Criteria

10/28/2021

Westinghouse IR-

21-12181

Re-Inspection of Flatness for ISFSI Pad

11/06/2021

Westinghouse IR-

21-13392

PINGP ISFSI Concrete Pad Thickness Variations

2/13/2021

Westinghouse IR-

21-6629

Soil Densometer Calibration Results Delta

06/11/2021

Corrective Action

Documents

Westinghouse IR-

21-8876

Braun Intertec Plate Load Test Data Loss

08/16/2021

501000056098

ISFSI Worker Stumbled on Rebar

09/16/2021

Corrective Action

Documents

Resulting from

Inspection

501000059767

ISFSI Exp. - Errors in Concrete Tickets

01/14/2022

Engineering

Changes

601000000444

ISFSI Expansion Project

Braun Intertec Co. Letter: Plate Load Test Results

08/17/2021

60853

Miscellaneous

S&L Review of Braun's "Plate Load Test Results - Braun

08/25/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Letter;"

FCR 001

PINGP ISFSI Pad Expansion - Excavation Work Plan

05/30/2021

FCR 002

PINGP ISFSI Pad Expansion - Excavation Work Plan

06/03/2021

FCR 003

PINGP ISFSI Pad Expansion - Excavation Work Plan

06/03/2021

FCR 005

PINGP ISFSI Pad Expansion - Excavation Work Plan

06/08/2021

FCR 006

PINGP ISFSI Pad Expansion - Excavation Work Plan

07/14/2021

FCR 019

PINGP ISFSI Pad Expansion - Pad Installation Work Plan

10/13/2021

FCR 020

Prairie Island ISFSI Pad Expansion - Pad Installation Work

Plan

10/13/2021

FCR 025

PINGP ISFSI Pad Expansion - Pad Installation Work Plan

11/06/2021

FCR 028

PINGP ISFSI Pad Expansion - Pad Installation Work Plan

11/09/2021

PO4500828442

Concrete Purchase Order

05/18/2021

ASTM D6951 Braun Intertec Quality Manual; MnDOT

Dynamic Cone Penetrometer Testing

Section 3.5.I.31

Braun Intertec Quality Manual; Potential Reactivity of

Aggregates - Mortar Bar Method

Procedures

Section 3.5.V.10

Braun Intertec Quality Manual; Moisture-Density Relation of

Soil-Modified Proctor

WO700081836

ISFSI Expansion: Concrete Pad Install

Work Orders

WO700082161

ISFSI Expansion: Excavation

2C1.5

Operation Without Computer

E-Plan

Emergency Plan

FP-EP-EQP-01

Equipment Important to Emergency Response

71111.04

Procedures

PINGP 1672, FP-

EP-EQP-01

Equipment Important to Emergency Response

Calculations

M-4163-001

C02 Concentrations in the Relay and Cable

Spreading/Computer Room

DBD Top 06

Design Bases Document for Fire Protection

Fire Plans

PINGP 1676

Unit #1 Hydrogen Seal Oil Unit Fire Drill and Critique

03/14/2022

71111.05

Work Orders

70100056221

SP 1275 10-Month Safe Shutdown Fire Barrier Inspection

08/14/2020

NF 39303-2

Miscellaneous Drain and Vent Piping

NF 39303-4

Miscellaneous Drain and Vent Piping-Unit 1

71111.06

Drawings

NF-39303

Miscellaneous Drain and Venting Pipe-Unit 1

06/30/1970

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

NF-39303-H3

Miscellaneous Drain and Vent Piping-Unit 1

06/30/1970

Engineering

Evaluations

EC: 0000008754

Evaluate the Relay and Cable Spreading Compartment for

Internal Flooding

Procedures

H36

Plant Flooding

Corrective Action

Documents

501000059179

One Year Turbine TE

2/17/2021

Engineering

Evaluations

1067-0096-LTR-

001

Prairie Island Turbine Valve Test Interval Extension

Evaluation (1 and 2)

01/07/2022

Maintenance Rule Expert Panel Meeting Minutes of

January 7, 2022

01/07/2022

Miscellaneous

Agenda

Prairie Island Maintenance Rule Expert Panel

Meeting - January 7, 2022

01/07/2022

5AWI 4.10.0

Technical Specification Bases and Technical Requirements

Manual Control Programs

Procedures

FP-E-MR-01

Maintenance Rule Process

71111.12

Work Orders

700095602

Troubleshooting Plan for C Kernel

01/05/2022

Corrective Action

Documents

501000060757

Group C PZR HTRs PRA Entry Time

2/22/2022

Procedures

H10.1

ASME Inservice Testing Program

71111.13

Work Orders

700007434

1-CL 7434 Clg Return HDR

2/28/2022

501000059495

Residual Heat Removal Voids

01/05/2022

501000059751

Operating Experience Evaluation (OEE) Westinghouse Tech

Bulletin 22-1: Reactor Coolant Pump (RCP) Casing Design

Analysis

01/13/2022

501000060104

"C" Phase Amperage Dropping 22 CD Pump

01/26/2022

Corrective Action

Documents

CE 501000058196

Conduct of Condition Evaluations (from FP-PA-ARP-01)

Frequency/Scope of GL-08-01 Locations Like

2RH-01/2RH-06

11/10/2021

2000019672

Troubleshooting Plan - Unit 2 Residual Heat Removal

System Voids

01/05/2022

608000000834

Review of Void at 2RH-14-500IN3-Part 1 (Void Loads)

608000000834

Review of Void at 2RH-14-500IN3-Part 2 (Structural

Investigation)

71111.15

Engineering

Evaluations

608000000834

Unit 2 Residual Heat Removal System - Void at 2RH-14

01/05/2022

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Operability

Evaluations

501000059495

(ECR

60800000000834)

Evaluation to Support Past Operability of Voiding on the

"B" Train of RHR

H10.1

ASME Inservice Testing Program

Procedures

SP 1106B

Diesel Cooling Water Pump Monthly Test

103

Work Orders

700102337

"C" Phase Voltage Dropping 22 CD Pump

2/08/2022

IP-ENG-001

Standard Design Process (EB-17-06)

Procedures

IP-ENG-001

Design Equivalent Change Package

700070278

D5 Fuel Oil Replacement Piping Coat - Activity 60

08/12/2021

71111.18

Work Orders

70100093990

D6 Vault Inspection UNS

01/18/2022

Procedures

SP 1106A

Diesel Cooling Water Pump Monthly Test

100

7000062859

2 CR/CU Fan Timer Faulty

2/16/2022

700007134

Wall Thinning Due to MIC-Repair/Replace

05/03/2021

700007434

Post Maintenance Testing 6" Piping - Wall Thinning Due to

MIC - Repair/Replacement

05/03/2021

70001029610010

Replace D6 E1 Gov Actuator

2/07/2022

700062859

2CR C/U Fan Timer Faulty - Bench Test Replacement

Timer

2/17/2022

700102961

Replace D6 E1 Governor Actuator

2/07/2022

71111.19

Work Orders

701000062590020

2 CR/CU Fan Timer Faulty

2/16/2022

501000020741

NOS: F5 App K Cardox System and Doors 56/57

2/05/2018

Corrective Action

Documents

501000061537

Turbine Valve Leak

03/22/2022

Drawings

NF-39335-185

Residual Heat Removal A-73-97

11/10/1971

Procedures

SP 2468.01

Unit 2 GL-08-01 Inspections for Mode 1, 3, and 4

700079294

SP 1194 18-Month Cardox (CO2) Systems Test

01/05/2022

700092505

SP 2089A-2A Residual Heat Removal Pump and Suction

Valve From RWST

01/28/2022

70090687

SP 2856 BUS 26 Undervoltomnicron Test

01/18/2022

70100091894

SP 2095 BUS 26 Load Sequencer Test

01/18/2022

71111.22

Work Orders

WO 700101720

SP 2468.1 Unit 2 GL-08-01 Inspections for Modes 1, 3,

and 4

01/18/2022

71152S

Corrective Action

501000059609

AST NRC RAI Response Incorrect

01/10/2022

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

501000059748

NRC Violation Partial ACE Request

01/13/2022

Documents

501000060402

Update NRC Response

2/07/2022

501000056770

Incorrect Information Provided to the NRC

10/05/2021

Corrective Action

Documents

Resulting from

Inspection

501000057560

Rev 8 of PTLR Submitted with Errors

10/21/2021

ENG-ME-819

Adjusted Reference Temperatures for Unit 1 and Unit 2

Reactor Vessel Materials at 54 EFPY

SIR-99-75

Update to the Generic Letter 92-01 Reactor Vessel

Structural Integrity for Prairie Island Units 1 and 2

2

Calculations

WCAP-14637

Prairie Island Unit 2 Heat up and Cooldown Limit Curves for

Normal Operation

Corrective Action

Documents

500001473878

Reactor Vessel Fluence Calculations

04/11/2015

Corrective Action

Documents

Resulting from

Inspection

501000060322

NRC Question Fluence Methodology Change

2/03/2022

71153

Procedures

H44

Reactor Vessel Integrity Program

2