ML11213A091

From kanterella
Jump to navigation Jump to search
IR 05000461-11-003, on 04/01/11 - 06/30/11, Clinton Power Station, Unit 1, Heat Sink Performance, Surveillance Testing
ML11213A091
Person / Time
Site: Clinton Constellation icon.png
Issue date: 07/29/2011
From: Ring M
NRC/RGN-III/DRP/B1
To: Pacilio M
Exelon Generation Co, Exelon Nuclear
References
IR-11-003
Download: ML11213A091 (62)


See also: IR 05000461/2011003

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION III

2443 WARRENVILLE ROAD, SUITE 210

LISLE, IL 60532-4352

July 29, 2011

Mr. Michael J. Pacilio

Senior Vice President, Exelon Generation Company, LLC

President and Chief Nuclear Officer (CNO), Exelon Nuclear

4300 Winfield Road

Warrenville, IL 60555

SUBJECT: CLINTON POWER STATION, NRC INTEGRATED INSPECTION REPORT

05000461/2011-003

Dear Mr. Pacilio:

On June 30, 2011, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at

your Clinton Power Station. The enclosed report documents the inspection results, which were

discussed on July 13, 2011, with Mr. W. Noll and other members of your staff.

This inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, two NRC-identified findings of very low safety

significance were identified. Both of these findings were determined to involve violations of

NRC requirements. Additionally, one licensee-identified violation, which was determined to be

of very low safety significance, was reviewed by the inspectors and is listed in this report.

Because of the very low safety significance and because they were entered into your

corrective action program, the NRC is treating the above inspector-identified and

licensee-identified violations as non-cited violations (NCVs) consistent with Section VI.A.1 of

the NRC Enforcement Policy. If you contest any NCV, you should provide a response within

30 days of the date of this inspection report, with the basis for your denial to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001;

with copies to the Regional Administrator, Region III; the Director, Office of Enforcement,

U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident

Inspector at Clinton Power Station. In addition, if you disagree with the cross-cutting aspect

assigned to any finding in this report in this report, you should provide a response within

30 days of the date of this inspection report, with the basis for your disagreement to the

Regional Administrator, Region III, and the NRC Resident Inspector at Clinton Power Station.

The information you provide will be considered in accordance with Inspection Manual

Chapter 0305.

M. Pacilio -2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter,

its enclosure, and your response (if any) will be available electronically for public inspection in

the NRC Public Document Room or from the Publicly Available Records System (PARS)

component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Website

at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Mark A. Ring, Chief

Branch 1

Division of Reactor Projects

Docket No. 50-461

License No. NPF-62

Enclosure: Inspection Report 05000461/2011-003

w/Attachment: Supplemental Information

cc w/encl: Distribution via ListServ

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket No: 50-461

License No: NPF-62

Report No: 05000461/2011-003

Licensee: Exelon Generation Company, LLC

Facility: Clinton Power Station, Unit 1

Location: Clinton, IL

Dates: April 1 through June 30, 2011

Inspectors: B. Kemker, Senior Resident Inspector

D. Lords, Resident Inspector

C. Brown, Reactor Inspector

J. Cassidy, Senior Health Physicist

A. Dunlop, Senior Reactor Engineer

M. Jones Jr., Reactor Inspector

R. Winter, Reactor Inspector

S. Mischke, Resident Inspector, Illinois Emergency

Management Agency

Approved by: M. Ring, Chief

Branch 1

Division of Reactor Projects

Enclosure

TABLE OF CONTENTS

SUMMARY OF FINDINGS ......................................................................................................... 1

REPORT DETAILS .................................................................................................................... 3

Summary of Plant Status ........................................................................................................ 3

1. REACTOR SAFETY..................................................................................................... 3

1R01 Adverse Weather Protection (71111.01) ........................................................... 3

1R04 Equipment Alignment (71111.04)...................................................................... 5

1R05 Fire Protection (71111.05) ................................................................................ 6

1R06 Flooding Protection Measures (71111.06) ........................................................ 7

1R07 Heat Sink Performance (71111.07)................................................................... 8

1R11 Licensed Operator Requalification Program (71111.11) ..................................11

1R12 Maintenance Effectiveness (71111.12) ............................................................11

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13) .......12

1R15 Operability Evaluations (71111.15) ..................................................................13

1R18 Plant Modifications (71111.18) ........................................................................14

1R19 Post-Maintenance Testing (71111.19) .............................................................14

1R22 Surveillance Testing (71111.22) ......................................................................15

1EP6 Drill Evaluation (71114.06) ..............................................................................21

2. RADIATION SAFETY ..................................................................................................22

2RS3 In-Plant Airborne Radioactivity Control and Mitigation (71124.03) ...................22

2RS4 Occupational Dose Assessment (71124.04) ....................................................26

4. OTHER ACTIVITIES ...................................................................................................30

4OA1 Performance Indicator Verification (71151) ......................................................30

4OA2 Identification and Resolution of Problems (71152) ...........................................31

4OA3 Followup of Events and Notices of Enforcement Discretion (71153) ................32

4OA5 Other Activities ................................................................................................33

4OA6 Management Meetings ....................................................................................37

4OA7 Licensee-Identified Violations ..........................................................................38

SUPPLEMENTAL INFORMATION............................................................................................. 1

KEY POINTS OF CONTACT .................................................................................................. 1

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED........................................................ 2

LIST OF DOCUMENTS REVIEWED ...................................................................................... 4

LIST OF ACRONYMS USED.................................................................................................17

Enclosure

SUMMARY OF FINDINGS

IR 05000461/2011-003, 04/01/11 - 06/30/11, Clinton Power Station, Unit 1, Heat Sink

Performance, Surveillance Testing.

This report covers a three-month period of inspection by the resident inspectors and announced

baseline inspections by regional inspectors. Two Green findings, both of which had an

associated non-cited violation, were identified. The significance of most findings is indicated by

their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609,

Significance Determination Process (SDP). Findings for which the SDP does not apply may

be Green or be assigned a severity level after NRC management review. The NRCs program

for overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.

A. NRC-Identified and Self-Revealed Findings

Cornerstone: Mitigating Systems

Criterion III, Design Control, having very low safety significance for the failure to

include all of the applicable heat loads in the Reactor Core Isolation Cooling (RCIC)

Room heat up calculation and not having a calculation of record for the RCIC Room heat

up under a station blackout (SBO) scenario. The licensee entered this issue into the

corrective action program and performed preliminary calculations to verify that the issues

did not exceed any design limits.

The performance deficiency was determined to be more than minor because it

was associated with the Mitigating Systems Cornerstone attribute of Equipment

Performance, and affected the cornerstone objective of ensuring the availability,

reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences. The finding screened as very low safety significance

because the licensee determined the RCIC Room cooler was capable of removing the

additional heat load; and RCIC Room temperature remained within the design limits

without the room cooler during a SBO scenario. The inspectors determined that this

finding did not represent current licensee performance and no cross-cutting aspect was

assigned. (Section 1R07.1.b.(1))

Cornerstone: Initiating Events

  • Green. The inspectors identified a finding of very low safety significance (Green) with an

associated non-cited violation of Technical Specification Surveillance Requirement

(TSSR) 3.4.6.1. The licensee failed to correctly incorporate the required test pressure

limits of the TSSR into the surveillance test procedure and subsequently tested multiple

reactor coolant system (RCS) pressure isolation valves (PIVs) at pressures greater than

the maximum test pressure of 1025 pounds per square inch gauge, invalidating the

testing. The licensee performed a risk assessment of the missed surveillance in

accordance with TSSR 3.0.3, which determined that completion of the surveillance could

be delayed up to the 24-month surveillance interval without a significant increase in plant

risk. The licensee also completed an operability evaluation for the TS nonconformance

and concluded that there was reasonable assurance that the affected RCS PIVs were

operable based on engineering judgment.

1 Enclosure

The finding was of more than minor significance because it affected the Initiating Events

Cornerstone and was associated with the Procedure Quality attribute. Specifically, the

licensee did not correctly incorporate the required test pressure limits of TSSR 3.4.6.1

into the surveillance test procedure. This resulted in testing multiple RCS PIVs at

pressures greater than the maximum test pressure of 1025 psig. The finding was

determined to be a licensee performance deficiency of very low safety significance

because the finding would not result in exceeding the TS limit for RCS leakage and

would not have likely affected mitigation systems resulting in a loss of safety function.

The inspectors concluded that because the licensees missed opportunity to correct the

test pressure discrepancy in its surveillance test procedure occurred in January 2005

and no other more recent opportunities reasonably existed to identify and correct the

problem, this issue would not be reflective of current licensee performance and no

cross-cutting aspect was identified. (Section 1R22.b.(1))

B. Licensee-Identified Violations

A violation of very low safety significance that was identified by the licensee has been

reviewed by the inspectors. Corrective actions planned or taken by the licensee have

been entered into the licensees corrective action program. The violation and corrective

action tracking numbers are listed in Section 4OA7 of this report.

2 Enclosure

REPORT DETAILS

Summary of Plant Status

The unit was operated at or near full power during the inspection period with the following

exceptions:

On April 2, 2011, the licensee reduced power to about 48 percent (%) to perform repairs on a

main condenser tube leak. The unit was returned to full power the following day.

On April 8, 2011, the licensee reduced power to about 82% to perform control rod pattern

adjustments. The unit was returned to full power the same day.

On May 22, 2011, the licensee reduced power to about 80% to perform control rod sequence

exchange, scram time testing and recovery of two control rods following hydraulic control unit

maintenance, control rod settle testing, and main turbine control/stop/intermediate valve and

main steam isolation valve testing. The unit was returned to full power the same day.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01)

.1 Readiness For Impending Hot Summer Weather Conditions

a. Inspection Scope

The inspectors evaluated the licensees preparations for hot summer weather conditions,

focusing on the electrical distribution system and the plant chilled water system.

During the weeks of May 23, 2011, and June 20, 2011, the inspectors performed a

detailed review of severe weather and plant de-winterization procedures and performed

general area plant walkdowns. The inspectors focused on plant-specific design features

and implementation of procedures for responding to or mitigating the effects of hot

summer weather conditions on the operation of the plant. The inspectors reviewed

system health reports and system engineering summer readiness review documents for

the above systems.

Additionally, the inspectors verified that adverse weather related issues were entered

into the licensees corrective action program with the appropriate characterization and

significance. Selected action requests were reviewed to verify that corrective actions

were appropriate and implemented as scheduled.

This inspection constituted one seasonal extreme weather readiness inspection sample

as defined in Inspection Procedure (IP) 71111.01.

b. Findings

No findings were identified.

3 Enclosure

.2 Summer Readiness of Offsite and Alternate Alternating Current (AC) Power Systems

a. Inspection Scope

The inspectors evaluated the licensees plant features and procedures for operation and

continued availability of offsite and alternate AC power systems. The inspectors

interviewed plant personnel and reviewed the licensees communications protocols

between the Transmission System Operator (TSO) and the plant to verify that the

appropriate information was being exchanged when issues arose that could impact the

offsite power system. Aspects considered in the inspectors review included:

  • The actions to be taken when notified by the TSO that the post-trip voltage of the

offsite power system at the plant will not be acceptable to assure the continued

operation of the safety related loads without transferring to the onsite power

supply;

  • The compensatory actions identified to be performed if it is not possible to predict

the post-trip voltage at the plant for the current grid conditions;

  • The required re-assessment of plant risk based on maintenance activities that

could affect grid reliability, or the ability of the transmission system to provide

offsite power; and

  • The required communications between the plant and the TSO when changes at

the plant could impact the transmission system, or when the capability of the

transmission system to provide adequate offsite power is challenged.

The inspectors performed a walkdown of the switchyard with a plant maintenance

engineer to observe the material condition of the offsite power sources. The inspectors

also reviewed the status of outstanding work orders to assess whether corrective actions

for any degraded conditions were scheduled with the TSO with the appropriate priority.

This inspection constituted one offsite and alternate AC power systems readiness

inspection sample as defined in IP 71111.01.

b. Findings

No findings were identified.

.3 Readiness For Impending Adverse Weather Condition - Tornado/High Winds

a. Inspection Scope

Since thunderstorms with potential tornados and high winds were forecast in the vicinity

of the facility for the week of April 18, 2011, the inspectors reviewed the licensees

overall preparations/protection for the expected conditions. The inspectors toured the

plant grounds in the vicinity of the main power transformers, unit auxiliary transformer,

reserve auxiliary transformers, emergency reserve auxiliary transformer, and static volt

amp reactive compensators to look for loose debris, which if present could become

missiles during a tornado or with high winds. During the inspections, the inspectors

focused on plant-specific design features and the licensees procedure used to respond

to tornado and high winds conditions.

4 Enclosure

This inspection constituted one readiness for impending adverse weather condition

inspection sample as defined in IP 71111.01.

b. Findings

No findings were identified.

.4 Readiness to Cope with External Flooding

a. Inspection Scope

The inspectors reviewed flood protection barriers and procedures for coping with

external flooding at the plant. The Clinton Power Station has limited susceptibility to

external flooding as described in Section 3.4.1.1 of the Updated Final Safety Analysis

Report (UFSAR) and Section 5.2 of the Individual Plant Examination for External Events

Report. The inspectors reviewed CPS 4303.02, Abnormal Lake Level, Revision 10, to

assess the adequacy of the licensee response to external flooding conditions.

The inspectors conducted a walkdown of the Lake Screen House, including the

shutdown service water pump rooms. The inspectors assessed the condition of water

tight door seals; the sealing of equipment floor plugs, electrical conduits, holes or

penetrations in floors and walls between the pump rooms; and the condition of room

floor drains, sumps, and sump pumps.

Additionally, the inspectors verified that external flooding protection issues were entered

into the licensees corrective action program with the appropriate characterization and

significance. Selected action requests were reviewed to verify that corrective actions

were appropriate and implemented as scheduled.

This inspection constituted one external flooding readiness inspection sample as defined

in IP 71111.01.

b. Findings

No findings were identified.

1R04 Equipment Alignment (71111.04)

.1 Quarterly Partial System Walkdowns (71111.04Q)

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

  • Standby Gas Treatment (VG) System Train B during planned maintenance on

VG System Train A;

  • Control Room Ventilation (VC) System Train B during planned maintenance on

VC System Train A; and

  • AC Power Distribution System (selected portions of risk-significant system).

5 Enclosure

The inspectors selected these systems based on their risk significance relative to the

Reactor Safety Cornerstones. The inspectors reviewed operating procedures, system

diagrams, Technical Specification (TS) requirements, and the impact of ongoing work

activities on redundant trains of equipment. The inspectors verified that conditions did

not exist that could have rendered the systems incapable of performing their intended

functions. The inspectors also walked down accessible portions of the systems to verify

system components were aligned correctly and available as necessary.

In addition, the inspectors verified that equipment alignment problems were entered into

the licensees corrective action program with the appropriate characterization and

significance. Selected action requests were reviewed to verify that corrective actions

were appropriate and implemented as scheduled.

This inspection constituted three partial system walkdown inspection samples as defined

in IP 71111.04.

b. Findings

No findings were identified.

1R05 Fire Protection (71111.05)

.1 Routine Resident Inspector Tours (71111.05Q)

a. Inspection Scope

The inspectors performed fire protection tours in the following plant areas:

  • Fire Zone A-1e, General Access Area (West) - Elevation 7370;
  • Fire Zone R-1j, Dry Active Waste Baler Room - Elevation 737'0";
  • Fire Zone R-1n, Paint and Oil Storage Room - Elevation 737'0"; and
  • Fire Zone T-1k, General Access Area (West) - Elevation 781'0".

The inspectors verified that transient combustibles and ignition sources were

appropriately controlled and assessed the material condition of fire suppression

systems, manual fire fighting equipment, smoke detection systems, fire barriers and

emergency lighting units. The inspectors verified that fire hoses and extinguishers were

in their designated locations and available for immediate use; that fire detectors and

sprinklers were unobstructed; that transient material loading was within the analyzed

limits; that the licensees fire plan was in alignment with actual conditions; and that fire

doors, dampers, and penetration seals appeared to be in satisfactory condition.

In addition, the inspectors verified that fire protection related problems were entered into

the licensees corrective action program with the appropriate characterization and

significance. Selected action requests were reviewed to verify that corrective actions

were appropriate and implemented as scheduled.

This inspection constituted four quarterly fire protection inspection samples as defined in

IP 71111.05AQ.

6 Enclosure

b. Findings

No findings were identified.

.2 Fire Protection - Drill Observation (71111.05A)

a. Inspection Scope

During an announced drill on May 26, 2011, associated with a simulated fire in the

Condensate Booster Pump Room, the inspectors assessed the timeliness of the

fire brigade in arriving at the scene, the fire fighting equipment brought to the scene,

the donning of fire protective clothing, the effectiveness of communications, and the

exercise of command and control by the fire brigade leader. The inspectors also

assessed the acceptance criteria for the drill objectives; the rigor and thoroughness of

the post-drill critique; and verified that fire protection drill issues were being entered into

the licensee's corrective action program with the appropriate characterization and

significance.

This inspection constituted one annual fire protection drill inspection sample as defined

in IP 71111.05AQ.

b. Findings

No findings were identified.

1R06 Flooding Protection Measures (71111.06)

.1 Internal Flooding

a. Inspection Scope

The inspectors reviewed selected risk important plant design features and licensee

procedures intended to protect the plant and its safety-related equipment from internal

flooding events. The inspectors reviewed flood analyses and design documents,

including the UFSAR, engineering calculations, and abnormal operating procedures to

identify licensee commitments. In addition, the inspectors reviewed licensee drawings to

identify areas and equipment that may be affected by internal flooding caused by the

failure or misalignment of nearby sources of water, such as the fire suppression or the

service water systems. The inspectors also reviewed the licensees corrective action

documents with respect to past flood-related items identified in the corrective action

program to verify the adequacy of the corrective actions. The inspectors performed a

walkdown of the following plant areas to assess the adequacy of watertight doors and

verify drains and sumps were clear of debris and were operable, and that the licensee

complied with its commitments:

  • Turbine Building Basement - Elevation 7020.

This inspection constituted one internal flooding inspection sample as defined in

IP 71111.06.

7 Enclosure

b. Findings

No findings were identified.

1R07 Heat Sink Performance (71111.07)

.1 Annual Heat Sink Performance (71111.07A)

a. Inspection Scope

The inspectors reviewed the licensees maintenance activities for the Division 2

Inverter Room cooler (1VX13SB). Specifically, the review included the program for

testing and analysis of the room cooler, which was cleaned, inspected, and evaluated.

The inspectors assessed the as-found and as-left condition of the heat exchanger by

direct observation and document reviews to verify that no deficiencies existed that would

adversely impact the heat exchangers ability to transfer heat to the shutdown service

water system and to ensure that the licensee was adequately addressing problems that

could affect the performance of the heat exchanger. The inspectors observed portions

of inspection and cleaning activities, and reviewed documentation to verify that the

inspection acceptance criteria specified in procedure ER-AA-340-1002, Service Water

Heat Exchanger Inspection Guide, Revision 4, were satisfactorily met.

This inspection constituted one annual heat sink inspection sample as defined in

IP 71111.07.

b. Findings

No findings were identified.

.2 Triennial Review of Heat Sink Performance (71111.07T)

a. Inspection Scope

The inspectors reviewed operability determinations, completed surveillances, vendor

manual information, associated calculations, performance test results and cooler

inspection results associated with the Reactor Core Isolation Cooling (RCIC) Room

cooler and Control Room chillers. These heat exchangers/coolers were chosen based

on their risk significance in the licensees probabilistic safety analysis, their important

safety-related mitigating system support functions, their operating history, and their

relatively low margin.

For the RCIC Room cooler and the Control Room chillers, the inspectors reviewed the

methods and results of heat exchanger performance inspections. The inspectors

verified the methods used to inspect and clean heat exchangers were consistent with

as-found conditions identified and expected degradation trends and industry standards,

the licensees inspection and cleaning activities had established acceptance criteria

consistent with industry standards, and the as-found results were recorded, evaluated,

and appropriately dispositioned such that the as-left condition was acceptable.

In addition, the inspectors verified the condition and operation of the RCIC Room cooler

and the Control Room chillers were consistent with design assumptions in heat transfer

calculations and as described in the UFSAR. This included verification that the number

8 Enclosure

of plugged tubes was within pre-established limits based on capacity and heat transfer

assumptions. The inspectors verified the licensee evaluated the potential for water

hammer and established adequate controls and operational limits to prevent heat

exchanger degradation due to excessive flow-induced vibration during operation.

In addition, eddy current test reports and visual inspection records were reviewed to

determine the structural integrity of the heat exchanger.

The inspectors also witnessed the inspection of the RCIC Room cooler to look for

indications of macrofouling that includes live or dead mussels and clams, plant

material, or silt.

The inspectors verified the performance of the ultimate heat sink (UHS) and

safety-related shutdown service water (SX) system and their subcomponents, such as

piping, intake screens, pumps, valves, etc., by tests or other equivalent methods to

ensure availability and accessibility to the in-plant cooling water systems.

The inspectors reviewed completed surveillances, associated calculations, buried pipe

inspection results, chemistry monitoring program, sedimentation monitoring procedures,

condition reports, and work orders to ensure the condition of the UHS and the

SX system.

The inspectors also verified pipe stress analyses, direct and indirect buried pipe

inspection test results, pump vibration data, and trends associated with the SX system to

ensure that acceptance criteria were being satisfied and the as-found inspection results

were recorded, evaluated, and appropriately dispositioned, such that the as left condition

was acceptable.

The inspectors also conducted walkdowns of the service water intake structure and the

SX Pump Rooms to verify the general condition of the system and associated

subsystems.

b. Findings

(1) Deficiencies with RCIC Room Heat Up Analyses

Introduction

A finding of very low safety significance and associated non-cited violation of 10 CFR 50,

Appendix B, Criterion III, Design Control, was identified by the inspectors for the failure

to include all of the applicable heat loads in the RCIC Room heat up calculation under

loss-of-coolant-accident (LOCA) and not having a calculation of record for the RCIC

room heat up under a station blackout (SBO) scenario.

Description

The inspectors reviewed calculation VY-01, VY System Cooling Load Calculation,

to verify the RCIC Room cooler was capable of removing heat generated in the RCIC

Room under various scenarios and that the room temperature would remain within the

design limit of 180 degrees Fahrenheit (°F). The inspectors identified that the RCIC

water leg pump was not listed as one of the rooms heat sources for several scenarios,

including LOCA and shutdown conditions. Although the heat load associated with the

pumps motor was small, under LOCA conditions, the available calculated margin was

only 4.6%.

9 Enclosure

In addition, the inspectors requested the analysis of the RCIC Room under an SBO

scenario. The licensee determined that this analysis had been inadvertently deleted

from calculation 3C10-1088-001, Revision 4, SBO Coping Assessment. As such there

was no calculation of record to address this scenario.

The licensee initiated action request (AR) 01206227 to address these concerns.

Based on the 5 horsepower RCIC water leg pump motor, the licensee determined there

was a 3% increase in heat load for the room, which reduced the available margin to

approximately 1.7%. During the licensees review, they also identified two

conservatisms in the calculation where pipe temperatures were assumed to be higher

than the temperatures that would be experienced during the scenario. Removal of these

conservatisms could increase the available margin to approximately 10%. With respect

to the SBO scenario, the licensee used the methodology in the calculation inputting

conservative room heat up loads and verified that the room temperature would be 157°F,

which was below the 180°F limit.

The inspectors concluded that, based on these evaluations, the RCIC Room

temperature would remain within the required limits during the various scenarios.

Analysis

The inspectors determined that the failure to include all heat loads in the RCIC Room

heat up calculations and to have a calculation of record for the RCIC Room heat up

under an SBO scenario was a performance deficiency. The performance deficiency was

determined to be more than minor because it was associated with the Mitigating

Systems Cornerstone attribute of Equipment Performance, and affected the cornerstone

objective of ensuring the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences. Specifically, the RCIC Room

heat up calculation did not include the RCIC water leg pump motor, which would have

added an additional 3% heat load reducing the available margin to 1.7%. In addition,

no calculation of record existed for the RCIC Room heat up under an SBO scenario to

verify the room would remain within the design temperature limits.

The inspectors determined the finding could be evaluated using the Significance

Determination Process (SDP) in accordance with IMC 0609, Significance Determination

Process, Attachment 0609.04, Phase 1 - Initial Screening and Characterization of

Findings, Table 4a for the Mitigating System Cornerstone. The finding screened as

very low safety significance (Green) because the finding was not a design or

qualification deficiency, did not represent a loss of system safety function, and did not

screen as potentially risk significant due to a seismic, flooding, or severe weather

initiating event. In addition, the licensee performed preliminary calculations to verify that

the RCIC Room cooler was capable of removing the additional heat load; and the RCIC

Room temperature remained within the design limits without the room cooler during a

SBO scenario.

Cross-Cutting Aspects

The inspectors determined there was no cross-cutting aspect associated with this finding

because this was a legacy design issue and, therefore, was not reflective of current

performance.

10 Enclosure

Enforcement

10 CFR 50, Appendix B, Criterion III, Design Control, requires, in part, that measures

shall be established to assure that applicable regulatory requirements and the design

basis are correctly translated into specifications, drawings, procedures, and instructions.

Contrary to the above, as of April 22, 2011, the licensee did not correctly translate

applicable regulatory requirements and the design basis into specifications and

procedures. Specifically, the RCIC Room heat up calculation did not include the RCIC

water leg pump motor heat load and there was no analysis for the RCIC Room heat up

under an SBO scenario. Because this violation was of very low safety significance and it

was entered into the licensees corrective action program as AR 01206227, this violation

is being treated as an non-cited violation consistent with Section 2.3.2 of the NRC

Enforcement Policy (NCV 05000461/2011003-01, Deficiencies with RCIC Room

Heat Up Analyses).

1R11 Licensed Operator Requalification Program (71111.11)

.1 Resident Inspector Quarterly Review (71111.11Q)

a. Inspection Scope

The inspectors observed licensed operators during simulator training on June 22, 2011.

The inspectors assessed the operators response to the simulated events focusing on

alarm response, command and control of crew activities, communication practices,

procedural adherence, and implementation of Emergency Plan requirements.

The inspectors also observed the post-training critique to assess the ability of licensee

evaluators and operating crews to self-identify performance deficiencies. The crews

performance in these areas was compared to pre-established operator action

expectations and successful critical task completion requirements.

This inspection constituted one quarterly licensed operator requalification inspection

sample as defined in IP 71111.11.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness (71111.12)

a. Inspection Scope

The inspectors evaluated the licensee's handling of selected degraded performance

issues involving the following risk-significant structures, systems, and components

(SSCs):

  • Radiation Monitoring System.

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the SSCs. Specifically, the inspectors independently verified

the licensee's handling of SSC performance or condition problems in terms of:

11 Enclosure

  • Appropriate work practices;
  • Identifying and addressing common cause failures;
  • Characterizing SSC reliability issues;
  • Tracking SSC unavailability;
  • Trending key parameters (condition monitoring);
  • Appropriateness of performance criteria for SSC functions classified (a)(2) and/or

appropriateness and adequacy of goals and corrective actions for SSC functions

classified (a)(1).

In addition, the inspectors verified that problems associated with the effectiveness of

plant maintenance were entered into the licensee's corrective action program with the

appropriate characterization and significance. Selected action requests were reviewed

to verify that corrective actions were appropriate and implemented as scheduled.

This inspection constituted one maintenance effectiveness inspection sample as defined

in IP 71111.12.

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a. Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for

maintenance and emergent work activities affecting risk-significant and safety related

equipment listed below to verify that the appropriate risk assessments were performed

prior to removing equipment for work:

  • Planned maintenance during the week of April 11-15 on the Division 2 Diesel

Generator (DG) and SX System;

  • Planned maintenance during the week of May 2-6 on the RCIC System;
  • Planned maintenance during the week of May 31-June 3 on the Division 1

Automatic Depressurization System, Division 1 VG System, Removal of Control

Building Tornado Missile Barrier, and Division 1 Essential Switchgear Heat

Removal System; and

  • Emergent maintenance during week of June 13-17 to address steam leaks in the

Turbine Building Heater Bay.

These activities were selected based on their potential risk significance relative to

the Reactor Safety Cornerstones. As applicable for each of the above activities, the

inspectors reviewed the scope of maintenance work in the plants daily schedule,

reviewed Control Room logs, verified that plant risk assessments were completed as

required by 10 CFR 50.65(a)(4) prior to commencing maintenance activities, discussed

the results of the assessment with the licensees Probabilistic Risk Analyst and/or Shift

Technical Advisor, and verified that plant conditions were consistent with the risk

assessment assumptions. The inspectors also reviewed TS requirements and walked

12 Enclosure

down portions of redundant safety systems, when applicable, to verify that risk analysis

assumptions were valid, that redundant safety related plant equipment necessary to

minimize risk was available for use, and that applicable requirements were met.

In addition, the inspectors verified that maintenance risk related problems were

entered into the licensees corrective action program with the appropriate significance

characterization. Selected action requests were reviewed to verify that corrective

actions were appropriate and implemented as scheduled.

This inspection constituted four maintenance risk assessment inspection samples as

defined in IP 71111.13.

b. Findings

No findings were identified.

1R15 Operability Evaluations (71111.15)

a. Inspection Scope

The inspectors reviewed the following issues:

[Pressure Isolation Valve] Surveillance Testing;

Instrument;

  • AR 1208215, "1E21F303 Abnormal Flow/Indication During LPCS [Low Pressure

Core Spray] Clearance Hang."

The inspectors selected these potential operability issues based on the risk significance

of the associated components and systems. The inspectors verified that the conditions

did not render the associated equipment inoperable or result in an unrecognized

increase in plant risk. When applicable, the inspectors verified that the licensee

appropriately applied TS limitations, appropriately returned the affected equipment to an

operable status, and reviewed the licensees evaluation of the issue with respect to the

regulatory reporting requirements. Where compensatory measures were required to

maintain operability, the inspectors determined whether the measures in place would

function as intended and were properly controlled. The inspectors determined, where

appropriate, compliance with bounding limitations associated with the evaluation.

In addition, the inspectors verified that problems related to the operability of

safety-related plant equipment were entered into the licensees corrective action

program with the appropriate characterization and significance. Selected action

requests were reviewed to verify that corrective actions were appropriate and

implemented as scheduled.

This inspection constituted five operability evaluation inspection samples as defined in

IP 71111.15.

13 Enclosure

b. Findings

No findings were identified.

1R18 Plant Modifications (71111.18)

.1 Temporary Modifications

a. Inspection Scope

The inspectors reviewed the following temporary plant modification:

for the Division I Diesel Governor.

The inspectors reviewed the temporary modification and the associated 10 CFR 50.59

screening/evaluation against applicable system design basis documents, including the

UFSAR and the TS to verify whether applicable design basis requirements were

satisfied. The inspectors reviewed the Control Room logs and interviewed engineering

and operations department personnel to understand the impact that implementation of

the temporary modification had on operability and availability of the affected plant SSCs.

This inspection constituted one temporary modification inspection sample as defined in

IP 71111.18.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing (71111.19)

a. Inspection Scope

The inspectors reviewed post-maintenance testing for the following activities to verify

that procedures and test activities were adequate to ensure system operability and

functional capability:

1TCVP013;"

LOCA Bypass Relay 3KL4;

1E51F030;

(1E51-F079 and F081 only).

The inspectors reviewed the scope of the work performed and evaluated the adequacy

of the specified post-maintenance testing. The inspectors verified that the

14 Enclosure

post-maintenance testing was performed in accordance with approved procedures; that

the procedures contained clear acceptance criteria, which demonstrated operational

readiness and that the acceptance criteria was met; that appropriate test instrumentation

was used; that the equipment was returned to its operational status following testing;

and, that the test documentation was properly evaluated.

In addition, the inspectors verified that problems related to post-maintenance testing

were entered into the licensees corrective action program with the appropriate

characterization and significance. Selected action requests were reviewed to verify that

corrective actions were appropriate and implemented as scheduled.

This inspection constituted seven post-maintenance testing inspection samples as

defined in IP 71111.19.

b. Findings

No findings were identified.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors reviewed the results of the following surveillance testing activities to

determine whether risk-significant systems and equipment were capable of performing

their intended safety function and to verify that the testing was conducted in accordance

with applicable procedural and TS requirements:

  • CPS 3822.06, Operation of the Horizontal Fire Pump; (Routine Test)
  • CPS 9070.01, Control Room HVAC [Heating, Ventilation and Air Conditioning]

Air Filter Package Operability Test Run; (Routine Test)

  • CPS 9051.02, HPCS Valve Operability Test; (Inservice Test)
  • CPS 9054.01, RCIC System Operability Checks; (Inservice Test) and
  • CPS 9053.04, "RHR [Residual Heat Removal] A/B/C Valve Operability Checks."

(Inservice Test)

The inspectors observed selected portions of the test activities to verify that the testing

was accomplished in accordance with plant procedures. The inspectors reviewed the

test methodology and documentation to verify that equipment performance was

consistent with safety analysis and design basis assumptions, and that testing

acceptance criteria were satisfied.

In addition, the inspectors verified that surveillance testing problems were entered into

the licensees corrective action program with the appropriate characterization and

significance. Selected action requests were reviewed to verify that corrective actions

were appropriate and implemented as scheduled.

This inspection constituted three in-service tests and two routine surveillance tests for a

total of five inspection samples as defined in IP 71111.22.

15 Enclosure

b. Findings

(1) Failure to Meet Surveillance Testing Requirement for Reactor Coolant System (RCS)

Pressure Isolation Valves (PIVs)

(Closed) Unresolved Item (URI)05000461/2011002-04, Reactor Coolant System

Pressure Isolation Valve Leakage Surveillance Test Procedure Questions

Introduction

The inspectors identified a finding of very low safety significance (Green) with an

associated non-cited violation of TS Surveillance Requirement (TSSR) 3.4.6.1.

The licensee failed to correctly incorporate the required test pressure limits of the TSSR

into the surveillance test procedure and subsequently tested multiple RCS PIVs at

pressures greater than the maximum test pressure of 1025 pounds per square inch

gauge (psig), invalidating the testing.

Discussion

The inspectors reviewed the licensees performance of surveillance testing that was

accomplished in accordance with CPS 9843.01, ISI [Inservice Inspection] Category A

Valve Leak Rate Test, Revision 35. This surveillance test procedure was performed to

satisfy TSSR 3.4.6.1, which required the licensee to verify the equivalent leakage of

each RCS PIV is 0.5 gallon-per-minute (gpm) per nominal inch of valve size up to a

maximum of 5 gpm, at an RCS pressure 1000 psig and 1025 psig in accordance

with the Inservice Testing Program. The licensees Inservice Testing Program specified

testing these valves once every 24-month refueling cycle during an outage.

As described in the Bases for TS 3.4.6.1, the main purpose in establishing a leakage

limit for the RCS PIVs is to prevent overpressure failure of the low pressure portions of

connecting systems. The leakage limit is an indication of whether the PIVs between the

RCS and the connecting systems are degraded or degrading.

During review of CPS 9843.01 and the completed test packages for RCS PIV testing

performed during the last refueling outage, the inspectors noted that much of the testing

was performed at pressures greater than the TSSR 3.4.6.1 maximum test pressure of

1025 psig. The procedure had the test performers calculate a corrected test pressure to

adjust for the elevation differences between the test gage and the valves undergoing

testing. This appeared to be appropriate in order to account for an actual pressure

difference at the valves as read from the test pressure gage to assure that the valves

would be tested at the correct pressure. However, the inspectors found that the test

procedure did not ensure that leakage testing was performed within the 1000-1025 psig

range specified by TSSR 3.4.6.1. Instead of calculating both an upper and a lower test

pressure based on the TSSR 3.4.6.1 limiting pressure range, the procedure had the test

performers calculate only one test pressure based on the maximum limit of 1025 psig.

Step 8.2.4 of the procedure directed the test performers to pressurize the test volume to

1025 psig (+25/-0 psig), rather than 1025 psig (-25/+0 psig). During review of the

completed test packages, the inspectors noted that, not accounting for calculation errors,

test performers pressurized the test volume to the calculated test pressure (+25/-0 psig).

The inspectors noted that the Bases for TS 3.4.6 states that leakage testing at a lower

pressure differential than between the specified maximum RCS pressure and the normal

16 Enclosure

pressure of the connected system during RCS operation (the maximum pressure

differential) is allowed. The observed rate may be adjusted to the maximum pressure

differential by assuming leakage is directly proportional to the pressure differential to the

one-half power. However, the inspectors found that the test procedure did not make any

allowance by way of calculating a corrected leakage for a lower pressure differential.

The inspectors also found no allowance in the TS Bases or in the procedure for testing

with a higher pressure differential.

The inspectors discussed these observations with the licensee and questioned whether

the required test pressure limits of TSSR 3.4.6.1 had been correctly incorporated into

the surveillance test procedure. The inspectors opened URI 05000461/2011002-04

pending additional review and resolution of open questions to determine whether the

surveillance test procedure was adequate to satisfy the surveillance testing requirement.

The licensee initiated action requests AR 01202456 and AR 01212825 to address the

inspectors questions.

In response to the inspectors questions, the licensee discovered that five RCS PIVs

(1E12-F023, 1E12-F042A, 1E12-F042C, 1E21-F006, and 1E22-F005) had been tested

at test pressures greater than the maximum 1025 psig limit specified in TSSR 3.4.6.1.

This resulted in invalid surveillance testing results for these five valves. The inspectors

noted that since the surveillance test procedure was incorrect, it was simply by chance

that only five of the RCS PIVs were found to have been tested above 1025 psig after the

licensee re-calculated corrected test pressures. The licensee performed a risk

assessment of the missed PIV surveillances in accordance with TSSR 3.0.3, which

determined that completion of the surveillances could be delayed up to the 24-month

surveillance interval without a significant increase in plant risk. The inspectors reviewed

the risk assessment and concurred that there was no unacceptable increase in risk.

The licensee also completed an operability evaluation for the TS nonconformance and

concluded that there was reasonable assurance that the affected PIVs were operable

based on engineering judgment. Although there was no defined relationship available to

equate valve seating force to valve seat leakage, the licensee concluded that the

relatively small change (decrease) in seating force due to a relatively small increase in

test pressure above the maximum test pressure would not result in a significant increase

in valve seat leakage such that the limiting leakage rates for the valves would not be

exceeded. The inspectors reviewed the operability evaluation and concluded that the

licensees conclusion was reasonable. The highest corrected test pressure calculated

for a PIV was 7.8 psi higher than the TSSR maximum test pressure.

The inspectors reviewed the licensees apparent cause evaluation for the missed

surveillance. The licensees evaluation highlighted that a missed opportunity to correct

the test pressure discrepancy had occurred in 2005. In December 2004, AR 00282084

was written to identify that the surveillance test procedure would test the RCS PIVs at

pressures up to 25 psig above the maximum pressure specified in TSSR 3.4.6.1.

However, the licensees subsequent evaluation of the described condition completed in

January 2005 was incorrect, in that, it concluded that testing at the higher pressure was

conservative and therefore acceptable. A change was made to CPS 9843.01 as an

enhancement to the procedure to add an explanatory statement accounting for the

apparent test pressure discrepancy. Step 2.1.11 of the test procedure stated, in part,

that [t]o conservatively ensure compliance with TSSR 3.4.6.1 test pressure

requirements, functional differential pressures are established at or above the upper

bound of pressure defined by TSSR 3.4.6.1, recognizing that TSSR 3.4.6.1 Bases state

17 Enclosure

that RCS PIV leakage is directly proportional to pressure to the 1/2 power. However,

according to the Bases for TS 3.4.6 this allowance is only for leakage testing at a lower

pressure differential between the specified maximum RCS pressure and the normal

pressure of the connected system during RCS operation.

The licensee identified that the apparent cause for the incorrect test pressure

specified in the surveillance test procedure was due to a technical human error.

Engineering judgment that testing at a higher pressure was conservative was not

challenged as being outside the literal test pressure band specified in the TSSR.

The inspectors reviewed AR 00282084 and noted that multiple licensee staff had

accepted this flawed engineering judgment, both in Engineering and Operations.

Corrective actions identified by the licensee included changes to CPS 9843.01 to

correct identified discrepancies with the test conditions and acceptance criteria.

In addition, to address a broader issue highlighted by this and other recent inspection

findings involving test control issues, the licensee identified an action from AR 01207467

to evaluate the generic issue involving translation of licensing/design basis requirements

into test procedures. The inspectors considered these corrective actions to be

appropriate.

The licensee stated in the apparent cause evaluation that the technical human error was

made in 2005, prior to the issuance of procedure HU-AA-1212, Technical Task

Risk/Rigor Assessment, Pre-job Brief, Independent Third Party Review, and Post-job

Review, which requires additional measures to be taken to identify assumptions during

engineering work. Therefore, the licensee did not identify any additional corrective

actions to address why the errors were made in the evaluation of AR 00282084.

Analysis

The inspectors determined that the licensees failure to satisfy the surveillance testing

requirement to verify the equivalent leakage of each RCS PIV is 0.5 gpm per nominal

inch of valve size up to a maximum of 5 gpm, at an RCS pressure 1000 psig and

1025 psig was a performance deficiency warranting a significance evaluation.

The inspectors reviewed the examples of minor issues in IMC 0612, Power Reactor

Inspection Reports, Appendix E, Examples of Minor Issues, and found no examples

related to this issue. Consistent with the guidance in IMC 0612, Power Reactor

Inspection Reports, Appendix B, Issue Screening, the inspectors determined that the

finding affected the Initiating Events Cornerstone and was associated with the Procedure

Quality attribute. Specifically, the licensee did not correctly incorporate the required test

pressure limits of TSSR 3.4.6.1 into the surveillance test procedure. This resulted in

testing multiple RCS PIVs at pressures greater than the maximum test pressure of

1025 psig. The inspectors performed a Phase 1 SDP review of this finding using the

guidance provided in IMC 0609, Attachment 0609.04, Phase 1 - Initial Screening and

Characterization of Findings. In accordance with Table 4a, Characterization

Worksheet for IE [Initiating Events], MS [Mitigating Systems], and BI [Barrier Integrity]

Cornerstones, the inspectors determined that that this finding was a licensee

performance deficiency of very low safety significance (Green) because the finding

would not result in exceeding the TS limit for RCS leakage and would not have likely

affected mitigation systems resulting in a loss of safety function. Based on consultation

and review with the Regional Senior Reactor Analyst, the inspectors concluded that the

18 Enclosure

testing deficiency did not result in an increase in valve failure probability or the likelihood

of an initiating event such as an inter-system LOCA.

Cross-Cutting Aspects

The inspectors concluded that because the licensees missed opportunity to correct the

test pressure discrepancy in its surveillance test procedure occurred in January 2005

and no other more recent opportunities reasonably existed to identify and correct the

problem, this issue would not be reflective of current licensee performance and no

cross-cutting aspect was identified.

Enforcement

TSSR 3.4.6.1 requires the licensee to verify the equivalent leakage of each RCS PIV is

0.5 gpm per nominal inch of valve size up to a maximum of 5 gpm, at an RCS

pressure 1000 psig and 1025 psig in accordance with the Inservice Testing Program.

The licensees Inservice Testing Program specified testing these valves once every

24-month refueling cycle during an outage.

Contrary to the above, during surveillance testing between January 12 and 19, 2010,

performed in accordance with CPS 9843.01, ISI Category A Valve Leak Rate Test,

Revision 35, the licensee performed leakage testing of five RCS PIVs (1E12-F023,

1E12-F042A, 1E12-F042C, 1E21-F006, and 1E22-F005) at test pressures greater than

the maximum 1025 psig limit specified in TSSR 3.4.6.1. This resulted in invalid

surveillance testing results for these five valves for the previous 24-month refueling

cycle. Because of the very low safety significance, this violation is being treated as an

non-cited violation consistent with Section 2.3.2 of the NRC Enforcement Policy

(NCV 05000461/2011003-02, Failure to Meet Surveillance Testing Requirement for

Reactor Coolant System Pressure Isolation Valves). The licensee entered this

violation into its corrective action program as AR 01202456 and AR 01212825.

URI 05000461/2011002-04 is closed.

(2) Surveillance Testing of Control Room Ventilation (VC) System

Introduction

The inspectors initiated an Unresolved Item pending additional review and resolution of

open questions to determine whether the licensees VC system monthly operability

surveillance test procedure contained the appropriate requirements and acceptance

limits for intake filtered flow rate from applicable design documents and whether

operators appropriately addressed the operability of VC Train A after identifying a

degraded condition that could have affected the ability of the system to perform its safety

function.

Discussion

The inspectors reviewed the licensees performance of surveillance testing that was

accomplished in accordance with CPS 9070.01, Control Room HVAC Air Filter Package

Operability Test Run, Revision 26d. This surveillance test procedure was performed

to satisfy TSSRs 3.7.3.1 and 3.7.3.2, which required the licensee to operate each

19 Enclosure

VC subsystem with flow through the makeup filter 10 continuous hours with the heater

operating and with flow through the recirculation filter for 15 minutes, respectively.

The surveillance frequency is every 31 days. As described in the Bases for TS 3.7.3,

the ability of the VC system to maintain the habitability of the Control Room envelope is

an explicit assumption for the safety analyses presented in the UFSAR. The high

radiation mode of the VC system is assumed to operate following a design basis

accident. The VC system is designed to maintain a habitable environment in the

Control Room envelope for a 30-day continuous occupancy after a design basis

accident, without exceeding 5 Rem total effective dose equivalent (TEDE) as required

by 10 CFR 50, Appendix A, Criterion 19. The UFSAR Chapter 15 accident analyses

assumed that for a design basis LOCA, the VC system intake filtered flow rate is

3000 +/- 10% cubic feet per minute (cfm).

During testing of VC Train A on April 1, 2011, an operator noted that the filtered make

up flow was oscillating between 2300 and 2880 cfm; however, as stated in Step 8.1.2.h

of the test procedure, flow should have been 2700 to 3300 cfm. The operator annotated

the test procedure with a note stating that the flow was low and initiated AR 01196342 to

have the condition evaluated and corrected. Operators reviewed the acceptance criteria

in Section 9.1 of the test procedure and did not find any upper or lower limits for flow

rate. Operators noted that the Control Room differential pressure remained positive with

the degraded flow condition and, therefore, concluded that VC Train A remained

operable and signed off the completed test procedure as satisfactory with no further

evaluation. Operators did not request a formal operability evaluation from engineering

even though the VC system has a required licensing basis function and the degraded

condition could have affected the ability of the system to perform its safety function.

During review of the completed surveillance test procedure and AR 01196342, the

inspectors questioned: (1) whether VC Train A remained operable with intake filtered

flow less than design, and (2) the absence of an appropriate quantitative acceptance

criterion for filtered flow rate in the test procedure to assure that the system would be

capable of fulfilling its design safety function. The inspectors noted that TSSRs 3.7.3.1

and 3.7.3.2 do not specify upper or lower limits for system intake filtered flow rate, nor

do any other VC system TSSRs. Only the administrative program requirement for

VC system filter testing in TS 5.5.7 specifies a 3000 cfm intake filtered flow rate, but this

testing is performed much less frequently (i.e., every 2 years vice every month).

The inspectors reviewed CPS 9866.01, VG/VC HEPA [High Efficiency Particulate Air]

Filter Leak Test, Revision 26 and noted that this procedure for system filter testing

contained appropriate filtered flow acceptance criteria.

Because the UFSAR Chapter 15 LOCA analyses assumes that the VC system intake

filtered flow rate is 3000 +/- 10%, the inspectors determined that system operability would

be questionable with system flow not within these limits. For determining the radiological

consequences of a design basis LOCA to Control Room operators from external

radiation sources, Calculation C-002, Post LOCA Control Room Operator Dose from

External Sources, Revision 2, assumes the intake filtered flow rate is at the upper limit

of 3300 cfm. The higher value provides a maximum value for iodine buildup in the

charcoal bed under normal conditions. For determining the radiological consequences

of a design basis LOCA using the alternate source term methodology, Calculation

C-020, Reanalysis of Loss of Coolant Accident (LOCA) Using the Alternate Source

Term Methodology, Revision 3, assumes the intake filtered flow rate is 2700 cfm.

Under this analysis, the lower the flow rate the higher the dose to Control Room

20 Enclosure

operators since less filtered air is being provided to the Control Room envelope. Both of

the above calculations support the accident analyses to ensure that post accident dose

to Control Room occupants in the event of a LOCA would be less than 5 Rem TEDE.

The licensee investigated the low flow condition two weeks later on April 15th and

discovered that the VC Train A flow controller was not functioning properly. The flow

controller was replaced with a new one and post-maintenance testing was completed

satisfactorily. The licensee documented the flow controller problem in AR 012003343

and subsequently performed a past operability evaluation. The licensees evaluation

concluded that the system remained operable with the degraded flow condition because

there was sufficient margin in the Control Room post-LOCA dose analysis.

The inspectors reviewed the licensees evaluation and concluded that the results were

reasonable.

In response to the inspectors questions, the licensee initiated AR 01207896 to review

the absence of an appropriate quantitative acceptance criterion for filtered flow rate in

the surveillance test procedure. In addition, the licensee initiated AR 01239007 to

perform an apparent cause evaluation addressing the timeliness of the formal operability

assessment and whether the absence of appropriate acceptance criteria in Section 9.1

of CPS 9070.01 influenced the decision by licensed operators to accept the results of

the surveillance test and not request a formal operability evaluation from engineering

upon discovery of the degraded condition during testing.

At the end of this inspection period, the licensee had just entered this issue into its

corrective action program to investigate the cause and to identify appropriate corrective

actions. This issue is considered to be an Unresolved Item (URI 05000461/2011003-03,

Surveillance Testing of Control Room Ventilation System) pending additional review

and resolution of open questions to determine: (1) whether the surveillance test

procedure contained the appropriate requirements and acceptance limits for VC system

intake filtered flow rate from applicable design documents, and (2) whether operators

appropriately addressed the operability of VC Train A after identifying a degraded

condition that could have affected the ability of the system to perform its safety function.

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation (71114.06)

.1 Emergency Preparedness Drill Observation

a. Inspection Scope

The inspectors evaluated the conduct of an emergency preparedness drill on May 17,

2011, to identify any weaknesses and deficiencies in classification, notification, and

protective action recommendation development activities. This drill was planned to be

evaluated and was included in performance indicator data regarding drill and exercise

performance. The inspectors observed emergency response operations in the Technical

Support Center to determine whether the event classification, notifications, and

protective action recommendations were performed in accordance with procedures.

The operations simulator was not staffed for this drill. The inspectors also attended the

licensees drill critique to compare any inspector-observed weaknesses with those

identified by the licensees staff in order to evaluate the critique and to verify whether the

21 Enclosure

licensees staff was properly identifying weaknesses and entering them into the

corrective action program.

This inspection constituted one emergency preparedness drill evaluation inspection

sample as defined in IP 71114.06.

b. Findings

No findings were identified.

2. RADIATION SAFETY

Cornerstones: Occupational Radiation Safety

2RS3 In-Plant Airborne Radioactivity Control and Mitigation (71124.03)

This inspection constituted a partial sample as defined in IP 71124.03.

.1 Inspection Planning (02.01)

a. Inspection Scope

The inspectors reviewed the UFSAR to identify areas of the plant designed as potential

airborne radiation areas and any associated ventilation systems or airborne monitoring

instrumentation. Instrumentation review included continuous air monitors (continuous air

monitors and particulate-iodine-noble-gas-type instruments) used to identify changing

airborne radiological conditions such that actions to prevent an overexposure may be

taken. The review included an overview of the respiratory protection program and a

description of the types of devices used. The inspectors reviewed UFSAR, TS, and

emergency planning documents to identify location and quantity of respiratory protection

devices stored for emergency use.

Inspectors reviewed the licensees procedures for maintenance, inspection, and use of

respiratory protection equipment including self-contained breathing apparatus (SCBA) as

well as procedures for air quality maintenance.

The inspectors reviewed reported performance indicators to identify any related to

unintended dose resulting from intakes of radioactive material.

b. Findings

Introduction

The inspectors identified a discrepancy between the SCBA configuration and the

Operating and Instruction Manual. Specifically, the licensee procedure for maintaining

the respiratory equipment did not specify the authorized battery and the licensee used

batteries other than those specified in the Operating and Instruction Manual.

22 Enclosure

Discussion

The licensee used MSA MMR Air Mask with Firehawk Regulator SCBA units.

This model is National Institute for Occupational Safety and Health (NIOSH) approved

and includes a heads up display to inform the user of the amount of air remaining in the

tank through a series of light emitting diodes and is powered by a series of batteries.

The Operating and Instruction Manual includes the NIOSH approval for the equipment

as well as the cautions and limitations for that approval. Item N states that

Never substitute, modify, add, or omit parts. Use only exact replacement parts in the

configuration as specified by the manufacturer. The manufacturer includes a caution to

[U]se only Duracell NEDA 24A or Eveready NEDA 24AC AAA alkaline batteries. Use of

other batteries will void the Intrinsic Safety approval. Additionally, the heads up display

units were labeled with a similar message; however, the batteries listed were different.

Consequently there was another discrepancy between the SCBA Operating and

Instruction Manual and the manufacturer labeling on the equipment. The inspectors

identified that Rayovac batteries, not listed in the Operating and Instruction Manual or

the labels, were used in the SCBA units. The licensee was attempting to obtain

clarification from the manufacturer for the correct batteries and impact of using other

batteries. The issue remains under review by the NRC and is categorized as an

Unresolved Item pending completion of that revised evaluation and NRC review

(URI 05000461/2011003-04, NIOSH Approval of SCBAs).

.2 Engineering Controls (02.02)

a. Inspection Scope

The inspectors assessed whether the licensee had established trigger points

(e.g., the Electric Power Research Institutes Alpha Monitoring Guidelines for

Operating Nuclear Power Stations) for evaluating levels of airborne beta-emitting

(e.g., plutonium-241) and alpha-emitting radionuclides.

b. Findings

No findings were identified.

.3 Use of Respiratory Protection Devices (02.03)

a. Inspection Scope

The inspectors assessed whether respiratory protection devices used to limit the intake

of radioactive materials were certified by the National Institute for Occupational Safety

and Health/Mine Safety and Health Administration or have been approved by the

NRC per 10 CFR 20.1703(b).

The inspectors reviewed records of air testing for supplied-air devices and self-contained

breathing apparatus bottles to assess whether the air used in these devices meets or

exceeds Grade D quality. The inspectors reviewed plant breathing air supply systems to

determine whether they meet the minimum pressure and airflow requirements for the

devices in use.

23 Enclosure

The inspectors selected several individuals qualified to use respiratory protection

devices, and assessed whether they have been deemed fit to use the devices by a

physician.

The inspectors selected several individuals assigned to wear a respiratory protection

device and observed them donning, doffing, and functionally checking the device as

appropriate.

The inspectors chose multiple respiratory protection devices staged and ready for use

in the plant or stocked for issuance for use. The inspectors assessed the physical

condition of the device components (mask or hood, harnesses, air lines, regulators,

air bottles, etc.) and reviewed records of routine inspection for each. The inspectors

selected several of the devices and reviewed records of maintenance on the vital

components (e.g., pressure regulators, inhalation/exhalation valves, hose couplings).

b. Findings

No findings were identified.

.4 Self-Contained Breathing Apparatus for Emergency Use (02.04)

a. Inspection Scope

Based on the UFSAR, TS, and emergency operating procedure requirements, the

inspectors reviewed the status and surveillance records of SCBAs staged in-plant for

use during emergencies. The inspectors reviewed the licensees capability for refilling

and transporting SCBA air bottles to and from the Control Room and Operations Support

Center during emergency conditions.

The inspectors selected several individuals on Control Room shift crews and from

designated departments currently assigned emergency duties (e.g., onsite search and

rescue duties) to assess whether Control Room operators and other emergency

response and radiation protection personnel (assigned in-plant search and rescue duties

or as required by emergency operating procedures or the Emergency Plan) were trained

and qualified in the use of SCBAs (including personal bottle change out). The inspectors

evaluated whether personnel assigned to refill bottles were trained and qualified for that

task.

The inspectors determined whether appropriate mask sizes and types are available for

use (i.e., in-field mask size and type match what was used in fit-testing). The inspectors

determined whether on-shift operators had no facial hair that would interfere with the

sealing of the mask to the face and whether vision correction (e.g., glasses inserts or

corrected lenses) was available as appropriate.

The inspectors reviewed the past two years of maintenance records for select SCBA

units used to support operator activities during accident conditions and designated as

ready for service to assess whether any maintenance or repairs on any SCBA units

vital components were performed by an individual, or individuals, certified by the

manufacturer of the device to perform the work. The vital components typically are the

pressure-demand air regulator and the low-pressure alarm. The inspectors reviewed the

onsite maintenance procedures governing vital component work to determine any

24 Enclosure

inconsistencies with the SCBA manufacturers recommended practices. For those

SCBAs designated as ready for service, the inspectors determined whether the

required, periodic air cylinder hydrostatic testing was documented and up to date, and

the retest air cylinder markings required by the U.S. Department of Transportation were

in place.

b. Findings

Introduction

The inspectors identified missing spectacle kits for one licensed operator that was

required to wear corrective lenses while performing licensed activities. Licensee

procedure RP-AA-440, Respiratory Protection Program states, An individual who

requires vision correction and may need to wear full facepiece-type respirators is

required to obtain the appropriate lenses/spectacle kit, unless the individual is able to

wear contact lenses.

Discussion

Spectacle kits are corrective lenses designed to fit inside a respirator that allow the user

to wear corrective lenses without compromising the seal integrity of the respirator.

A user that requires corrective lenses to complete work activities and does not have a

spectacle kit could not perform the work while wearing the respirator. The licensee

maintains a central location for licensed operators to store spectacle kits and a separate

storage location for members of the fire brigade. These storage locations ensure that

the spectacle kits are centrally located to facilitate a rapid response when required

(fires, chemical spills, or other emergencies).

The licensee did not have a validation process to ensure that individuals who may need

to wear full face-piece-type respirators actually have the required spectacle kits.

The licensee indicated that a review/evaluation of this issue would be completed.

The issue remains under review by the NRC and is categorized as an Unresolved Item

pending completion of that revised evaluation and NRC review

(URI 05000461/2011003-05, Missing Respirator Spectacle Kits).

.5 Problem Identification and Resolution (02.05)

a. Inspection Scope

The inspectors evaluated whether problems associated with the control and mitigation of

in-plant airborne radioactivity were being identified by the licensee at an appropriate

threshold and were properly addressed for resolution in the licensee corrective action

program. The inspectors assessed whether the corrective actions were appropriate for a

selected sample of problems involving airborne radioactivity and were appropriately

documented by the licensee.

b. Findings

No findings were identified.

25 Enclosure

2RS4 Occupational Dose Assessment (71124.04)

This inspection constituted a partial sample as defined in IP 71124.04.

.1 Inspection Planning (02.01)

a. Inspection Scope

The inspectors reviewed the results of radiation protection program audits related to

internal and external dosimetry (e.g., licensees quality assurance audits,

self-assessments, or other independent audits) to gain insights into overall licensee

performance in the area of dose assessment and focus the inspection activities

consistent with the principle of smart sampling.

The inspectors reviewed the most recent National Voluntary Laboratory Accreditation

Program accreditation report on the vendors most recent results to determine the status

of the contractors accreditation.

A review was conducted of the licensee procedures associated with dosimetry

operations, including issuance/use of external dosimetry (routine, multi-badging,

extremity, neutron, etc.), assessment of internal dose (operation of whole body counter,

assignment of dose based on derived air concentration-hours, urinalysis, etc.), and

evaluation of and dose assessment for radiological incidents (distributed contamination,

hot particles, loss of dosimetry, etc.).

The inspectors evaluated whether the licensee had established procedural requirements

for determining when external and internal dosimetry is required.

b. Findings

No findings were identified.

.2 External Dosimetry (02.02)

a. Inspection Scope

The inspectors evaluated the onsite storage of dosimeters before their issuance, during

use, and before processing/reading. The inspectors also reviewed the guidance

provided to radiation workers with respect to care and storage of dosimeters.

The inspectors assessed whether non-National Voluntary Laboratory Accreditation

Program accredited passive dosimeters (e.g., direct ion storage sight read dosimeters)

were used according to licensee procedures that provide for periodic calibration,

application of calibration factors, usage, reading (dose assessment) and zeroing.

The inspectors assessed the use of active dosimeters (electronic personal dosimeters)

to determine if the licensee uses a correction factor to address the response of the

electronic personal dosimeter as compared to the passive dosimeter for situations when

the electronic personal dosimeter must be used to assign dose and whether the

correction factor is based on sound technical principles.

26 Enclosure

The inspectors reviewed dosimetry occurrence reports or corrective action program

documents for adverse trends related to electronic personal dosimeters, such as

interference from electromagnetic frequency, dropping or bumping, failure to hear

alarms, etc. The inspectors assessed whether the licensee had identified any trends

and implemented appropriate corrective actions.

b. Findings

No findings were identified.

.3 Internal Dosimetry (02.03)

Routine Bioassay (In Vivo)

a. Inspection Scope

The inspectors reviewed procedures used to assess the dose from internally deposited

nuclides using whole body counting equipment. The inspectors evaluated whether the

procedures addressed methods for differentiating between internal and external

contamination, the release of contaminated individuals, the route of intake, and the

assignment of dose.

The inspectors reviewed the whole body count process to determine if the frequency of

measurements was consistent with the biological half-life of the nuclides available for

intake.

The inspectors reviewed the licensee's evaluation for use of its portal radiation monitors

as a passive monitoring system to determine if instrument minimum detectable activities

were adequate to determine the potential for internally deposited radionuclides sufficient

to prompt additional investigation.

The inspectors selected several whole body counts and evaluated whether the counting

system used had sufficient counting time/low background to ensure appropriate

sensitivity for the potential radionuclides of interest. The inspectors reviewed the

radionuclide library used for the count system to determine its appropriateness.

The inspectors evaluated whether any anomalous count peaks/nuclides indicated in

each output spectra received appropriate disposition. The inspectors reviewed the

licensee's 10 CFR 61 data analyses to determine whether the nuclide libraries included

appropriate gamma-emitting nuclides. The inspectors evaluated how the licensee

accounts for hard-to-detect nuclides in the dose assessment.

b. Findings

No findings were identified.

Special Bioassay (In Vitro)

a. Inspection Scope

There were no internal dose assessments obtained using in vitro monitoring for the

inspectors to review. The inspectors reviewed and assessed the adequacy of the

licensees program for in vitro monitoring (i.e., urinalysis and fecal analysis) of

27 Enclosure

radionuclides (tritium, fission products, and activation products), including collection and

storage of samples.

The inspectors reviewed the vendor laboratory quality assurance program and assessed

whether the laboratory participated in an industry recognized cross-check program

including whether out-of-tolerance results were resolved appropriately.

b. Findings

No findings were identified.

Internal Dose Assessment - Airborne Monitoring

a. Inspection Scope

The inspectors reviewed the licensee's program for airborne radioactivity assessment

and dose assessment, as applicable, based on airborne monitoring and calculations of

derived air concentration. The inspectors determined whether flow rates and collection

times for air sampling equipment were adequate to allow lower limits of detection to be

obtained. The inspectors also reviewed the adequacy of procedural guidance to assess

internal dose if respiratory protection was used. The licensee had not performed dose

assessments using airborne/derived air concentration monitoring since the last

inspection.

b. Findings

No findings were identified.

Internal Dose Assessment - Whole Body Count Analyses

a. Inspection Scope

The inspectors reviewed several dose assessments performed by the licensee using the

results of whole body count analyses. The inspectors determined whether affected

personnel were properly monitored with calibrated equipment and that internal

exposures were assessed consistent with the licensee's procedures.

b. Findings

No findings were identified.

.4 Special Dosimetric Situations (02.04)

Declared Pregnant Workers

a. Inspection Scope

The inspectors assessed whether the licensee informed workers, as appropriate, of the

risks of radiation exposure to the embryo/fetus, the regulatory aspects of declaring a

pregnancy, and the specific process to be used for (voluntarily) declaring a pregnancy.

28 Enclosure

The inspectors selected individuals who had declared pregnancy during the current

assessment period and evaluated whether the licensees radiological monitoring

program (internal and external) for declared pregnant workers was technically adequate

to assess the dose to the embryo/fetus. The inspectors reviewed exposure results and

monitoring controls employed by the licensee with respect to the requirements of

10 CFR 20.

b. Findings

No findings were identified.

Dosimeter Placement and Assessment of Effective Dose Equivalent for External

Exposures

a. Inspection Scope

The inspectors reviewed the licensee's methodology for monitoring external dose in

non-uniform radiation fields or where large dose gradients exist. The inspectors

evaluated the licensee's criteria for determining when alternate monitoring, such as use

of multi-badging, was to be implemented.

The inspectors reviewed dose assessments performed using multi-badging to evaluate

whether the assessment was performed consistently with licensee procedures and

dosimetric standards.

b. Findings

No findings were identified.

Shallow Dose Equivalent

a. Inspection Scope

The inspectors reviewed shallow dose equivalent dose assessments for adequacy.

The inspectors evaluated the licensees method (e.g., VARSKIN or similar code) for

calculating shallow dose equivalent from distributed skin contamination or discrete

radioactive particles.

b. Findings

No findings were identified.

Neutron Dose Assessment

a. Inspection Scope

The inspectors evaluated the licensees neutron dosimetry program, including dosimeter

types and/or survey instrumentation.

The inspectors reviewed neutron exposure situations (e.g., independent spent fuel

storage installation operations or at-power containment entries) and assessed whether:

(a) dosimetry and/or instrumentation was appropriate for the expected neutron spectra;

29 Enclosure

(b) there was sufficient sensitivity for low dose and/or dose rate measurement; and

(c) neutron dosimetry was properly calibrated. The inspectors also assessed whether

interference by gamma radiation had been accounted for in the calibration and whether

time and motion evaluations were representative of actual neutron exposure events, as

applicable.

b. Findings

No findings were identified.

Assigning Dose of Record

a. Inspection Scope

For the special dosimetric situations reviewed in this section, the inspectors assessed

how the licensee assigns dose of record for total effective dose equivalent, shallow dose

equivalent, and lens dose equivalent. This included an assessment of external and

internal monitoring results, supplementary information on Individual exposures

(e.g., radiation incident investigation reports and skin contamination reports), and

radiation surveys and/or air monitoring results when dosimetry was based on these

techniques.

b. Findings

No findings were identified.

.5 Problem Identification and Resolution (02.05)

a. Inspection Scope

The inspectors assessed whether problems associated with occupational dose

assessment were being identified by the licensee at an appropriate threshold and

were properly addressed for resolution in the licensees corrective action program.

The inspectors assessed the appropriateness of the corrective actions for a selected

sample of problems documented by the licensee involving occupational dose

assessment.

b. Findings

No findings were identified.

4. OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

.1 Review of Submitted Quarterly Data

a. Inspection Scope

The inspectors performed a review of the data submitted by the licensee for the First

Quarter 2011 Performance Indicators for any obvious inconsistencies prior to its public

release in accordance with IMC 0608, "Performance Indicator Program."

30 Enclosure

This inspection was not considered to be an inspection sample as defined in IP 71151.

b. Findings

No findings were identified.

.2 Mitigating Systems Performance Index - Emergency Alternating Current (AC)

Power System

a. Inspection Scope

The inspectors reviewed a sample of plant records and data against the reported

Mitigating Systems Performance Index (MSPI) - Emergency AC Power System

Performance Indicator. To determine the accuracy of the performance indicator data

reported, performance indicator definitions and guidance contained in Nuclear Energy

Institute (NEI) 99-02, Regulatory Assessment Performance Indicator Guideline,

Revision 6, were used. The inspectors reviewed the MSPI derivation reports,

Control Room logs, Maintenance Rule database, Licensee Event Reports (LERs), and

maintenance and test data from July 2010 through March 2011, to validate the accuracy

of the performance indicator data reported. The inspectors reviewed the MSPI

component risk coefficient to determine if it had changed by more than 25% in value

since the previous inspection, and if so, that the change was in accordance with

applicable NEI guidance. The inspectors also reviewed the licensees corrective action

program database to determine if any problems had been identified with the

performance indicator data collected or transmitted for this performance indicator.

This inspection constituted one MSPI - Emergency AC Power System Performance

Indicator verification inspection sample as defined in IP 71151.

b. Findings

No findings were identified.

4OA2 Identification and Resolution of Problems (71152)

.1 Routine Review of Identification and Resolution of Problems

a. Inspection Scope

As discussed in previous sections of this report, the inspectors routinely reviewed issues

during baseline inspection activities and plant status reviews to verify that they were

being entered into the licensees corrective action program at an appropriate threshold,

that adequate attention was being given to timely corrective actions, and that adverse

trends were identified and addressed. Some minor issues were entered into the

licensees corrective action program as a result of the inspectors observations; however,

they are not discussed in this report.

This inspection was not considered to be an inspection sample as defined in IP 71152.

31 Enclosure

b. Findings

No findings were identified.

.2 Annual In-Depth Review Sample

a. Inspection Scope

The inspectors selected the following action request for in-depth review:

[Main Steam Line] A, B, and C Test Failure.

The inspectors verified the following attributes during their review of the licensee's

corrective actions for the above action requests and other related action requests:

  • Complete and accurate identification of the problem in a timely manner

commensurate with its safety significance and ease of discovery;

  • Consideration of the extent of condition, generic implications, common cause and

previous occurrences;

  • Evaluation and disposition of operability/reportability issues;
  • Classification and prioritization of the resolution of the problem, commensurate

with safety significance;

  • Identification of the root and contributing causes of the problem; and
  • Identification of corrective actions, which were appropriately focused to correct

the problem.

The inspectors discussed the corrective actions and associated action request

evaluation with licensee personnel.

This inspection constituted one annual in-depth review sample as defined in IP 71152.

b. Findings and Observations

No findings were identified.

4OA3 Followup of Events and Notices of Enforcement Discretion (71153)

.1 (Closed) LER 05000461/2009-005-01, Manual Scram on High Water Level Due to

Reactor Recirc [Recirculation] Pump Trip, Supplement 1

On October 15, 2009, Unit 1 was manually scrammed following an unexpected trip

of the B reactor recirculation pump. Operators manually scrammed the reactor just

before reactor vessel water level reached the Level 8 (high level) reactor scram set

point. After the unit was shut down, the licensee identified that the pump motor had

failed due to an internal electrical fault. The licensee reported this event in

LER 05000461/2009-005-00 as a condition that resulted in the manual actuation of the

reactor protection system in accordance with 10 CFR 50.73(a)(2)(iv)(A).

The performance issue related to this event was discussed in NRC Inspection Report

05000461/2010-002. The inspectors documented a finding of very low safety

significance as a result of the licensees failure to correct a non-conforming condition

32 Enclosure

with inadequate feedwater level control system response that resulted in a second

reactor scram for the same cause.

The licensee submitted Supplement 1 to the original LER to revise the cause for the

reactor vessel water level control issue and to update corrective actions that were

completed. The inspectors determined that the information provided in

LER 05000461/2009-005-01 did not change the conclusion of the previous review.

LER 05000461/2009-005-01 is closed.

This inspection constituted one event followup inspection sample as defined in IP 71153.

.2 (Closed) LER 05000461/2008-001-02, Reactor Recirc [Recirculation] Pump Trip

Initiates Automatic Scram on High RPV [Reactor Pressure Vessel] Water Level,

Supplement 2

On February 10, 2008, Unit 1 automatically scrammed following an unexpected trip of

the B reactor recirculation pump when reactor vessel water level reached the Level 8

(high level) reactor scram set point. The licensee reported this event in

LER 05000461/2008-001-00 and LER 05000461/2008-001-01 as a condition that

resulted in the automatic actuation of the reactor protection system in accordance with

10 CFR 50.73(a)(2)(iv)(A). The performance issues related to this event were discussed

in NRC Inspection Report 05000461/2008-004. The inspectors concluded that the

licensees failure to perform adequate post-maintenance testing (i.e., feedwater level

control system tuning) following the replacement of a feedwater level control system

dynamic compensator card during the Cycle 10 refueling outage in February 2006 was a

finding of very low safety significance. The inspectors also concluded that the licensees

failure to evaluate an unexpected and unknown cause for stray voltage in the

End-of-Cycle Recirculation Pump Trip circuit discovered during post-modification testing

during the Cycle 11 refueling outage in February 2008 was a finding of very low safety

significance.

The licensee submitted Supplement 2 to the original LER to revise the cause for the

reactor vessel water level control issue and to update corrective actions that were

completed. The inspectors determined that the information provided in

LER 05000461/2008-001-02 did not change the conclusion of the previous review.

LER 05000461/2008-001-02 is closed.

This inspection constituted one event followup inspection sample as defined in IP 71153.

4OA5 Other Activities

.1 (Closed) NRC Temporary Instruction (TI) 2515/183, Followup to the Fukushima Daiichi

Nuclear Station Fuel Damage Event

The inspectors assessed the activities and actions taken by the licensee to assess its

readiness to respond to an event similar to the Fukushima Daiichi Nuclear Plant fuel

damage event. This included: (1) an assessment of the licensees capability to mitigate

conditions that may result from beyond design basis events, with a particular emphasis

on strategies related to the spent fuel pool, as required by NRC Security Order

Section B.5.b issued on February 25, 2001, as committed to in Severe Accident

Management Guidelines, and as required by 10 CFR 50.54(hh); (2) an assessment of

33 Enclosure

the licensees capability to mitigate station blackout conditions, as required by

10 CFR 50.63 and station design bases; (3) an assessment of the licensees capability

to mitigate internal and external flooding events, as required by station design bases;

and (4) an assessment of the thoroughness of the walkdowns and inspections of

important equipment needed to mitigate fire and flooding events, which were performed

by the licensee to identify any potential loss of function of this equipment during seismic

events possible for the site.

Inspection Report 05000461/2011011 (ML111320336) documented detailed results of

this inspection activity.

.2 (Closed) NRC TI 2515/184, Availability and Readiness Inspection of Severe Accident

Management Guidelines (SAMGs)

On May 20, 2011, the inspectors completed a review of the licensees Severe Accident

Management Guidelines (SAMGs), implemented as a voluntary industry initiative in the

1990s, to determine (1) whether the SAMGs, were available and updated, (2) whether

the licensee had procedures and processes in place to control and update its SAMGs,

(3) the nature and extent of the licensees training of personnel on the use of SAMGs,

and (4) the licensee personnels familiarity with SAMG implementation.

The results of this review were provided to the NRC task force chartered by the

Executive Director for Operations to conduct a near-term evaluation of the need for

agency actions following the Fukushima Daiichi fuel damage event in Japan.

Plant-specific results for Clinton Power Station were provided as an Enclosure to a

memorandum to the Chief, Reactor Inspection Branch, Division of Inspection and

Regional Support, dated June 1, 2011, (ML111520396).

.3 (Closed) NRC TI 2515/177, Managing Gas Accumulation in Emergency Core Cooling,

Decay Heat Removal, and Containment Spray Systems (NRC Generic Letter 2008-01)

a. Inspection Scope

The inspectors verified that the onsite documentation, system hardware, and licensee

actions were consistent with the information provided in the licensees response to

NRC Generic Letter (GL) 2008-01, Managing Gas Accumulation in Emergency Core

Cooling (ECCS), Decay Heat Removal (DHR), and Containment Spray Systems.

Specifically, the inspectors verified that the licensee has implemented or was in the

process of implementing the commitments, modifications, and programmatically

controlled actions described in the licensees response to GL 2008-01. The inspection

was conducted in accordance with TI 2515/177, Managing Gas Accumulation in

Emergency Core Cooling, Decay Heat Removal, and Containment Spray Systems

(NRC Generic Letter 2008-01), and considered the site-specific supplemental

information provided by the Office of Nuclear Reactor Regulation (NRR) to the

inspectors.

The documents reviewed are listed in the Attachment to this report.

34 Enclosure

b. Inspection Documentation

The selected TI areas of inspection were licensing basis, design, testing, and corrective

actions. The documentation of the inspection effort and any resulting observations are

below.

Licensing Basis

The inspectors reviewed selected portions of licensing basis documents to verify that

they were consistent with the NRR assessment report and that they were processed by

the licensee. The licensing basis verification included the verification of selected

portions of TS, TS Bases, UFSAR, and Operations Requirements Manual. The

inspectors also verified that applicable documents that described the plant and plant

operation, such as calculations, piping and instrumentation diagrams (P&IDs),

procedures, and corrective action program documents, addressed the areas of concern

and were changed if needed following plant changes. The inspectors also confirmed

that the frequency of selected surveillance procedures were at least as frequent as

required by TSs. Finally, the inspectors confirmed that: (1) the licensee will review and

evaluate the resolution of TS issues with respect to the changes contained in the

Technical Specification Task Force (TSTF) traveler following NRC approval; and (2) that

a license amendment request will be submitted to the NRC within 180 days following the

evaluation, if necessary. The completion date for this regulatory commitment is

contingent upon the approval of the TSTF.

Design

The inspectors reviewed selected design documents, performed system walkdowns, and

interviewed plant personnel to verify that the design and operating characteristics were

addressed by the licensee. Specifically:

  • The inspectors assessed the licensees void acceptance criteria and noted that the

licensee established void volume acceptance criteria for piping locations located at

system high points to be used during field verifications. The void volumes were

derived based on pipe internal diameter and as-built slope, and internal height of the

void.

  • The inspectors selectively reviewed applicable documents, including calculations,

engineering evaluations, and vendor technical manuals, with respect to gas

accumulation in the residual heat removal (RHR) and high pressure core spray

(HPCS) systems. Specifically, the inspectors verified that these documents

addressed venting requirements, keep-full systems, and void control during system

realignments.

  • The inspectors conducted a walkdown of selected accessible portions of the RHR

system in sufficient detail to assess the licensees walkdowns. The inspectors also

verified that the information obtained during the licensees walkdown was consistent

with the items identified during the inspectors independent walkdown. In addition,

the inspectors verified that the licensee had P&IDs and isometric drawings that

describe the RHR system configurations and had confirmed the accuracy of the

drawings. The inspectors reviewed selected portions of isometric drawings and

considered the following:

35 Enclosure

a. High point vents were identified.

b. High points that do not have vents were recognizable.

c. Other areas where gas can accumulate and potentially impact subject system

operability, such as at orifices in horizontal pipes, isolated branch lines, heat

exchangers, improperly slopped piping, and under closed valves, were described

in the drawings or in referenced documentation.

d. Horizontal pipe centerline elevation deviations and pipe slopes in nominally

horizontal lines that exceed specified criteria were identified.

e. All pipes and fittings were clearly shown.

f. The drawings were up-to-date with respect to recent hardware changes and that

any discrepancies between as-built configurations and the drawings were

documented and entered into the corrective action program for resolution.

  • The inspectors also conducted similar walkdowns of selected inaccessible portions

of the HPCS system in other inspection periods. These additional activities counted

toward the completion of this TI and were documented in NRC Inspection Report

05000461/2010002.

  • The inspectors verified that licensee walkdowns have been completed. In addition,

the inspectors selectively verified that information obtained during the licensees

walkdowns was addressed and incorporated into procedures, the corrective actions

program, and the void management program.

Testing

The inspectors reviewed selected surveillance, post-modification test, and

post-maintenance test procedures and results to verify that the licensee has approved

and was using procedures that were adequate to address the issue of gas accumulation

and/or intrusion in the subject systems. This review included the verification of

procedures used for conducting surveillances and determination of void volumes to

ensure that the void criteria was satisfied and will be reasonably ensured to be satisfied

until the next scheduled void surveillance. Also, the inspectors reviewed procedures

used for filling and venting following conditions which may have introduced voids into the

subject systems to verify that the procedures addressed testing for such voids and

provided processes for their reduction or elimination. Additionally, the inspectors

reviewed ultrasonic test results for locations that were determined to be susceptible to

voiding based on the licensees walkdowns and evaluations.

The inspectors also review selected portions of procedures used during the surveillance

testing of subject systems in a separate inspection activity. This additional activity

counted towards the completion of this TI and was documented in NRC Inspection

Report 05000461/2010004.

Corrective Actions

The inspectors reviewed selected licensee assessment reports and corrective action

program documents to assess the effectiveness of the licensees corrective actions

36 Enclosure

when addressing the issues associated with GL 2008-01. The inspectors identified one

instance where the licensee failed to implement follow-up void management activities

when an action tracking item to resolve the issue was cancelled. Specifically, the

licensee cancelled a modification that was initiated to address a void identified in RHR

system piping with a horizontal centerline elevation deviation. When the modification

was cancelled, the licensee did not establish a follow-up void management activity.

The licensee performed a confirmatory ultrasonic examination and determined no void

existed. The licensee also issued AR 01212387 to document the inspectors concern of

canceling an action without evaluating the need for a substitute action.

In addition, the inspectors verified that selected corrective actions identified in the

licensees nine-month and supplemental reports were documented. The inspectors also

conducted a similar review of corrective action program documents in a separate

inspection activity. This additional activity counted towards the completion of this TI and

was documented in NRC Inspection Report 05000461/2010-004.

c. Findings

No findings were identified. Based on this review, the inspectors concluded that there is

reasonable assurance that the licensee will complete all outstanding items and

incorporate this information into the design basis and operational practices. Therefore,

this TI is considered closed.

4OA6 Management Meetings

.1 Resident Inspectors Exit Meeting

The inspectors presented the inspection results to Mr. W. Noll and other members of the

licensees staff at the conclusion of the inspection on July 13, 2011. The licensee

acknowledged the findings presented. Proprietary information was examined during this

inspection, but is not specifically discussed in this report.

.2 Interim Exit Meetings

Interim exit meetings were conducted for:

  • The results of NRC TI 2515/184, Availability and Readiness Inspection of Severe

Accident Management Guidelines (SAMGs), inspection with Mr. F. Kearney and

other members of the licensees staff at the conclusion of the inspection on

May 20, 2011. The inspector confirmed that none of the potential report input

discussed was considered proprietary.

  • The results of the Occupational Dose Assessment and In-Plant Airborne

Radioactivity Control and Mitigation inspection with Mr. F. Kearney and other

members of the licensees staff at the conclusion of the inspection on May 13, 2011,

and subsequently with Mr. J. Stovall on June 16, 2011. The inspector confirmed that

none of the potential report input discussed was considered proprietary.

  • The results of the Triennial Heat Sink and NRC TI 2515/177, Managing Gas

Accumulation in Emergency Core Cooling, Decay Heat Removal, and Containment

Spray Systems (NRC Generic Letter 2008-01), inspection with Mr. F. Kearney and

37 Enclosure

other members of the licensee staff on May 6, 2011, and subsequently with

Mr. R. Frantz on July 15, 2011. The inspectors confirmed that none of the potential

report input discussed was considered proprietary.

.3 Regulatory Performance Meeting

On April 28, 2011, the NRC held a meeting with the licensee at the Clinton Power

Station to discuss the Clinton Power Station annual plant performance assessment.

The assessment results were previously documented in Inspection Report

05000461/2011001.

.4 Public Meeting

On April 28, 2011, the NRC held a public open house meeting at the Clinton Elks Lodge

to engage interested members of the public on the performance of the Clinton Power

Station and the role of the NRC in ensuring safe plant operations upon completion of the

Clinton Power Station annual plant performance assessment in accordance with

Section 09.01 of IMC 0305, Operating Reactor Assessment Program.

4OA7 Licensee-Identified Violations

The following violation of very low significance (Green) was identified by the licensee

and is a violation of NRC requirements which meets the criteria of Section 2.3.2 of the

NRC Enforcement Policy, NUREG-1600, for being dispositioned as an non-cited

violation.

.1 Failure to Evaluate the Effects of Dynamic Loads on the Containment Spray Piping

Based on an issue identified at another facility, the licensee initiated AR 01197314 to

verify that the normally voided section of the RHR system containment spray piping

had been properly analyzed for dynamic loading during spray initiation. The licensee

determined that General Electric Design Specification 22A3139, Residual Heat

Removal, specified a dynamic loading analysis, which was required by American

Society of Mechanical Engineers Code,Section III, for the normally voided section of

piping; however, the licensee was unable to locate the analyses or justification for not

performing the analyses. The licensees initial evaluation as documented in calculation

3C10-0175-001, Design and Analysis of Clinton Containment Spray System, was

based on a review of Electric Power Research Institute Topical Report (TR)-106438,

Water Hammer Handbook for Nuclear Plant Engineers and Operators. The evaluation

concluded that a severe water hammer would not occur based on the condition that the

valves required to open were slow acting. However, the licensee determined the

evaluation was based on the case of a valve closing and not on the actual condition of

a valve opening and a slug of water moving through the voided section of pipe.

The licensee then performed an analysis of a water slug and confirmed the system

remained operable. Failure to have a dynamic loading analysis for this piping as

required by the design specification was considered a violation of 10 CFR 50,

Appendix B, Criterion III, Design Control. This violation was not greater than Green

because the dynamic loading was verified to be within the capability of the piping design.

ATTACHMENT: SUPPLEMENTAL INFORMATION

38 Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

K. Baker, Design Engineering Senior Manager

R. Campbell, RP Technical Specialist

T. Chalmers, Operations Director

C. Culp, Engineering

J. Cunningham, Security Manager

B. Davis, Regulatory Assurance Manager

J. Domitrovich, Work Management Director

C. Dunn, Shift Operations Superintendent

S. Fatora, Maintenance Director

R. Frantz, Regulatory Assurance

S. Gackstetter, Training Director

M. Heger, Mechanical/Structural Design Engineering Manager

N. Hightower, Radiological Engineering Manager

F. Kearney, Site Vice President

D. Kemper; Plant Engineering Senior Manager

A. Khanifar, Engineering Director

M. Kimmich, Engineering

S. Lakebrink, Mechanical Design Engineering

K. Leffel, Operations Support Manager

W. Noll, Site Vice President

J. Peterson, Regulatory Assurance

C. Rocha, Nuclear Oversight Manager

S. Soliman, Senior Chemist

J. Stovall, Radiation Protection Manager

B. Taber, Plant Manager

J. Ufert, Fire Marshall

T. Veitch, Chemistry Manager

1 Attachment

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Opened

05000461/2011-003-01 NCV Deficiencies with RCIC Room Heat Up Analyses

05000461/2011-003-02 NCV Failure to Meet Surveillance Testing Requirement for

Reactor Coolant System Pressure Isolation Valves

(Section 1R22.b.(1))

05000461/2011-003-03 URI Surveillance Testing of Control Room Ventilation System

(Section 1R22.b.(2))

05000461/2011-003-04 URI NIOSH Approval of SCBAs (Section 2RS3.1)

05000461/2011-003-05 URI Missing Respirator Spectacle Kits (Section 2RS3.4)

Closed

05000461/2011-003-01 NCV Deficiencies with RCIC Room Heat Up Analyses

05000461/2011-003-02 NCV Failure to Meet Surveillance Testing Requirement for

Reactor Coolant System Pressure Isolation Valves

(Section 1R22.b.(1))

05000461/2011-002-04 URI Reactor Coolant System Pressure Isolation Valve Leakage

Surveillance Test Procedure Questions (Section 1R22.b.(1))

05000461/2009-005-01 LER Manual Scram on High Water Level Due to Reactor Recirc

[Recirculation] Pump Trip, Supplement 1 (Section 4OA3.1)

05000461/2008-001-02 LER Reactor Recirc [Recirculation] Pump Trip Initiates Automatic

Scram on High RPV [Reactor Pressure Vessel] Water Level

(Section 4OA3.2)

2515/183 TI Followup to the Fukushima Daiichi Nuclear Station Fuel

Damage Event (Section 4OA5.1)

2515/184 TI Availability and Readiness Inspection of Severe Accident

Management Guidelines (SAMGs) (Section 4OA5.2)

2515/177 TI Managing Gas Accumulation in Emergency Core Cooling,

Decay Heat Removal, and Containment Spray Systems

(NRC Generic Letter 2008-01) (Section 4OA5.3)

Discussed

05000461/2009-005-00 LER Manual Scram on High Water Level Due to Reactor Recirc

[Recirculation] Pump Trip, Supplement 1 (Section 4OA3.1)

05000461/2010-002-05 FIN Failure to Correct Inadequate FWLCS Response Resulted in

High Reactor Vessel Water Level (Level 8) Scram

(Section 4OA3.1)

05000461/2008-001-00 LER Reactor Recirc [Recirculation] Pump Trip Initiates Automatic

Scram on High RPV [Reactor Pressure Vessel] Water Level

(Section 4OA3.2)

05000461/2008-001-01 LER Reactor Recirc [Recirculation] Pump Trip Initiates Automatic

Scram on High RPV [Reactor Pressure Vessel] Water Level

(Section 4OA3.2)

05000461/2008-004-01 FIN Failure to Perform Adequate Post-Maintenance Testing

Resulted in High Reactor Vessel Water Level (Level 8)

Scram (Section 4OA3.2)

2 Attachment

05000461/2008-004-02 FIN Failure to Evaluate an Unexpected and Unknown Cause for

Stray Voltage in the End-of-Cycle Recirculation Pump Trip

Circuit During Post-Modification Testing Resulted in a

Reactor Recirculation Pump Trip (Section 4OA3.2)

3 Attachment

LIST OF DOCUMENTS REVIEWED

The following is a list of documents reviewed during the inspection. Inclusion on this list does

not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that

selected sections of portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

1R01 Adverse Weather Protection

- OP-AA-108-111-1001, Severe Weather and Natural Disaster Guidelines, Revision

- OP-AA-106-101-1002, Exelon Nuclear Issues Management,

- CPS 4302.01, Tornado/High Winds, Revision 19a

- AR 01204822, Entry Into CPS 4302.01, Tornado/High Winds Off-Normal

- AR 01204927, 345 kV South Bus Voltage Low Out of Band

- AR 01204929, Two Storm Related Events

- OP-AA-106-101-1002, Exelon Nuclear Issues Management, Revision 8

- OP-AA-108-111-1001, Severe Weather and Natural Disaster Guidelines, Revision 5

- CPS 4302.01, Tornado/High Winds, Revision 19a

- CPS 4303.02, Abnormal Lake Level, Revision 10

- CPS 4304.01, Flooding, Revision 5a

- WC-AA-107, Seasonal Readiness, Revision 9

- AC-CD-1105-0001, Elevated Lake Temps Challenge CPS Operating Parameters,

May 9, 2011

- Letter from F. Kearney to B. Hanson, Subject: Certification of 2011 Summer Readiness,

May 15, 2011

- M05-1059, P&ID Floor & Equip. Drains Screen House (DM), Sheet 3, Revision L

- A22-1032, Circulating Water Screen House Main Floor Plan Area-12 - El. 6990, Revision K

- AR 01216152, Initiate ACMP for Summer Operation (IR 1091600)

- AR 01210375, Initiate ACMP for Elevated Lake Temp in Prep for Summer

- AR 01091600, ACMP Needed for High Lake Temperature

- AR 01215817, NER, NC-011-012 Seasonal Readiness/Tornado

- AR 01200986, 345 KV 4520 B Phase Disconnect Elevated in Temperature

- AR 01076285, Elevated Temperature on 0SY4504C Disconnect Ball Side

- AR 01101328, Possible Vulnerability to a Summer Fish Loss at CPS

- AR 01092236, Gaps Identified During Effectiveness Review [of Industry Event Report

Recommendation Implementation]

- AR 01158006, Weakness in Implementation of [Industry Event Report Recommendation]

- AR 01207940, NOS ID: Material Staged in North Parking Lot Not Secured

- AR 01200727, Grid Transient Causes GCB [Gas Circuit Breaker] 4510 to Cycle Open and

Shut

- AR 01183058, 345 KV Switchyard Walkdown Issues/Results From 3/3/2011

- AR 01219519, 345 KV Switchyard Walkdown 5/23/11

- AR 01224933, ERAT SVC HVAC Unit #2 0VV90SB Found Not Running

- AR 01224407, 0VV89SA: RAT SVC Building HVAC Compressor Tripped

- AR 01224783, Unit 2 RAT B SVC Building HVAC Unit Not Providing Cooling

- AR 01073472, Work Order Chiller C Amps Cycling

- AR 01219150, 0Work Order02CE Low Oil Pressure

- AR 01219249, 0Work Order02CA: A Work Order Chiller Trip on Low Oil Pressure

- AR 01201962, Main Generator Issues Requiring Attention

4 Attachment

1R04 Equipment Alignment

- -AR 010294475, Procedure Enhancement

- -CPS 9082.01, Offsite Source Power Verification, Revision 39b

- -E02-1AP03, Electrical Loading Diagram Clinton Power Station Unit 1, Revision AA

- -CPS 3319.01, Standby Gas Treatment (VG), Revision 16

- -CPS 3319.01V001, Standby Gas Treatment Valve Lineup, Revision 8

- -CPS 3319.01V002, Standby Gas Treatment Instrument Valve Lineup, Revision 5a

- -CPS 3319.01E001, Standby Gas Treatment Electrical Lineup, Revision 10c

- -M05-1105, P&ID Standby Gas Treatment System (VG), Sheet 1, Revision S

- -M05-1105, P&ID Standby Gas Treatment System (VG), Sheet 2, Revision N

- -M05-1105, P&ID Standby Gas Treatment System (VG), Sheet 3, Revision F

- CPS 3402.01, Control Room HVAC (VC), Revision 25c

- CPS 3402.01E001, Control Room HVAC Electrical Lineup, Revision 10b

- CPS 3402.01V001, Control Room HVAC Valve Lineup, Revision 16e

- M05-1102, Control Room HVAC (VC), Revision U

- E02-OVC99, Schematic Diagram, Control Room HVAC System (VC), Revision R

1R05 Fire Protection

- CPS 1893.04M003, Prefire Plan Legend, Revision 1

- CPS 1893.04M625, 737 RadWaste: Paint & Oil Storage Room Prefire Plan, Revision 4

- CPS 1893.04M730, 777, 781, 783 Turbine: General Access and Mezzanines Prefire Plan,

Revision 5

- Calculation IP-M-0177, Fire Loads in Clinton Power Station

- Work Order 01347983, Secondary Containment Door 1DR1-263 Has Damaged Seal, June

21, 2010

- AR 00790021, Potable Water Valve Leakby Prevents Clearance Order Work

- AR 01075728, Secondary Containment Door 1DR1-263 Has Damaged Seal

- AR 01209630, NRC Observations/Questions in 737 Fuel Building

- Clinton Power Station Updated Final Safety Analysis Report, Appendix E, Fire Protection

Evaluation Report - Clinton Power Station Unit 1, Revision 11

- Clinton Power Station Updated Final Safety Analysis Report, Appendix F, Fire Protection Safe

Shutdown Analysis - Clinton Power Station Unit 1, Revision 11

- OP-AA-201-009, Control of Transient Combustible Material, Revision 11

- OP-CL-201-009, Control of Transient Combustible Material, Revision 1

- CPS 1893.04M410, 737 Fuel: Grade Level Prefire Plan, Revision 4a

- CPS 1893.04M622, 737 Radwaste: Drum Area and Bailer Room Prefire Plan, Revision 4

1R06 Flooding Protection Measures

- CPS 4304.01, Flooding, Revision 5a

- CPS Individual Plant Examination (IPE), Section 3.3.8, Internal Flood Analysis,

September 1992

- CPS 3219.01, CT [Containment], AB [Auxiliary Building], FB [Fuel Building] Floor Drain (RF),

Revision 8

- CPS-PSA-012, Clinton PRA 2003 Update Internal Flooding Update: Integration of the Internal

Flooding Analysis into the Single-Top Model, Revision 0

- CPS 4411.03, Injection/Flooding Sources, Revision 7

- CC-AA-309-1001, Suppression Pool Equalization Levels, Revision 5

- Clinton Power Station Updated Safety Analysis Report, Revision 13

5 Attachment

- NRC Information Notice 2009-006, Construction-Related Experiences with Flood Protection

Features, July 21, 2009

- Calculation 3C10-0485-001, Internal Flooding Analysis, Revision 8, Volume B

- SL-4576, Internal Flooding - Safe Shutdown Analysis and INPO SOER No. 85-5 Comparison

Evaluation Report (Sargent & Lundy), January 31, 1990

- A22-1032, Circulating Water Screen House Main Floor Plan Area-12 - El. 6990, Revision K

- AR 01197979, Flood Seals Do Not Have Periodic Inspection Program

- AR 01197992, Temporary Materials For Flood Mitigation Not Routinely Inventoried

- AR 01197991, Valve Used In Internal Flood Mitigation Not Accessible

- AR 01197988, Fuses Called Out In CPS 4304.01 Are Not Segregated

- AR 01197987, Hatches On SX Roof For Flood Access Procedure Weakness

- AR 01196294, NRC Senior Resident Identified Need To Improve Leak Berm

- AR 01092206, Functionality Review of Condenser Pit Level Switch

- AR 01023891, 1LSTF001B Failed to Actuate Per 3813.01

1R07 Heat Sink Performance

- ER-AA-340-1002, Service Water Heat Exchanger Inspection Guide, Revision 4

- CPS 2602.01, Heat Exchanger Performance of Shutdown Service Water Coolers Covered by

NRC Generic Letter 89-13, Revision 16b

- CPS 8130.01, Heat Exchanger Maintenance/Repairs, Revision 3

- Calculation IP-M-0486, SX Acceptance Flows/Area Reductions, Revision 6C

- Work Order 01238289, Inspect, Boroscope, Clean, Eddy Current, and Hydrolase as Required

1VX13AB Coil, April 6, 2011

- Drawing MC-136-415B, Nuclear Containment Cooling Coil 1VX13AA AB,

- Catalog ID 1150970, Coil, Cooling, Cleanable Tube Water, Left Hand, Half Serpentine, 3

Rows, April 6, 2011

- AR 01169271, Triennial Heat Sink and GL 89-13 FASA Deficiency, January 31, 2011

- AR 778875, 2700.12, Not Complete within 5Y Frequency, May 23, 2008

- AR00797796, HVAC Calculation Temperature Inconsistency, July 17, 2008

- AR01095477, Initial Results from Div 1 SX Flow Balance, July 28, 2010

- AR01210756, 1VY04S - RCIC Room Cooler Airflow Exceeds Max Allowed, May 2, 2011

- Calculation No. 024429, Formal Piping Stress Analysis for Shutdown Service Water

Subsystem 1SX-51, September 23, 2008

- CPS 1003.10, Clinton Power Station (CPS) Program for NRC Generic Letter 89-13 (Service

Water Problems Affecting Safety-Related Equipment), Revision 6d

- CPS 1938.04, Raw Water Vendor Interface Procedure, Revision 4d

- CPS 3209.01, Raw Water Treatment (RWT) System, Revision 18b

- CPS 3211.01, Shutdown Service Water (SX), Revision 25e

- CPS 4303.02, Abnormal Lake Level, Revision 10

- CPS 6069.01D001, SX System Operability Data Sheet, Revision 45a

- CPS5050.06, High/Low Temp RCIC Pump Room, Revision 35

- CR No. 1-99-02-367, Shutdown Service Water Divisions 1 and 2 Made Inoperable during

Cross Connected Operation, February 23, 1999

- CR No: 1-98-11-006; Operating Procedures May Inappropriately Change Plant

Configuration, November 2, 1998

- CY-AA-120-4110, Raw Water Chemistry Strategic Plan, Revision 6

- EC 264758; Replacement of Div 2 expansion Joints 1SX01MB, 1SX02MB, 1SX03MB,

1SX04MB with Carbon Steel Pipe, December 6, 2010

- EC 372365, Installation of Insulating Gaskets for Division 1 DG Heat Exchanger Expansion

Joints, October 22, 2008

6 Attachment

- ER-AA-340-1001, GL 89-13 Program Implementation Instructional Guide, Revision 7

- ER-AA-5400, Buried Piping and Raw Water Corrosion Program (BPRWCP) Guide,

- Revision 4

- IP-M-0734, Shutdown Service Water (SX) System Divisions I and II Hydraulic Transient Load

Evaluation, EC 349061 and 358900, Revision 0

- Performance Trend Data for 1SX01-PA, PB, and PC, April 1, 2011

- VC-86, Evaluation of Control Room Chillers for Shutdown Service Water System, Revision 1

- VY-01, VY System Cooling Load Calculation, Revision 9C

- VY-45, Performance Evaluation of VY System Cooling Coils Under SX Flow Acceptance

Limits, Revision 4E

- VZ-43, Maximum Water Flow for Cooling Coils and Refrigeration Condenser Served by WS

System, Revision 1B

- VZ-45, SX Room Cooler Airflow Test Evaluation, Revision 0B

- WO 594629, Perform DIV II System Testing IAW 2700.13, April 8, 2008

- WO00789724; Inspect, Boroscope, Clean, Eddy Current and Hydrolase 1VY04A; May 5, 2009

- WO00859883, Obtain Air Flow Measurements for Room Cooler Coils 1VY04S,

August 9, 2007

- WO00864362, Major Inspection; Hydrolaze 0VC13CA Chiller, May 29, 2008

- WO01057470, Inspection/Clean Condenser; Hydrolance Tubes 0VC13CB Chiller,

November 12, 2008

- WO01195711, Div I SX System Testing IAW 2700.12, July 28, 2010

- WO01284960, Clean and Inspect 1VY04A Coil, May 3, 2011

1R12 Maintenance Effectiveness

- Regulatory Guide 1.160, Monitoring the Effectiveness of Maintenance at Nuclear Power

Plants, Revision 2 March 1997

- NUMARC 93-01, Industry Guideline for Monitoring the Effectiveness of Maintenance at

Nuclear Power Plants, Revision 2

- ER-AA-310, Implementation of Maintenance Rule, Revision 8

- ER-AA-310-1001, Maintenance Rule Scoping, Revision 4

- ER-AA-310-1005, Maintenance Rule - Dispositioning Between A(1) and A(2), Revision 5

- AR 00944238, 2)

- Clinton Power Station Updated Safety Analysis Report, Revision 13

- Regulatory Guide 1.160, Monitoring the Effectiveness of Maintenance at Nuclear Power

Plants, Revision 2 March 1997

- NUMARC 93-01, Industry Guideline for Monitoring the Effectiveness of Maintenance at

Nuclear Power Plants, Revision 2

- ER-AA-310, Implementation of Maintenance Rule, Revision 8

- ER-AA-310-1001, Maintenance Rule Scoping, Revision 4

- Maintenance Rule Scoping and Performance Criteria for Radiation Monitoring System,

May 23, 2011

- Common Cause Analysis 01179979, Potential Trend on Radiation Monitor Failures,

March 24, 2011

- AR 01179979, Potential Trend on Radiation Monitor Failures

- AR 01093695, 1RIX-PR042C Failed High

- AR 01090862, 1RIX-PR042B Failed Downscale to 0 Mr/Hr

- AR 01165170, 0RIX-PR001 High Range Noble Gas Channel Failed Calibration

- AR 01179569, 0RIX-PR001 Sample Pump Failed

- AR 01178074, 1RIX-PR006A High Alarm, Spike

7 Attachment

- AR 01204337, Received Unexpected AR/PR Hi Alarms on 1RIX-PR006A

- AR 01205697, 0RIX-PR004, SGTS Radiation Monitor in Communications Failure

1R13 Maintenance Risk Assessments and Emergent Work Control

- CPS 3310.01, Reactor Core Isolation Cooling (RI), Revision 27D

- CPS 9054.01, RCIC System Operability Check, Revision 43

- CPS 9054.01C001, RCIC Water Leg Pump 1E51-C003 Operability Test 1E51-F040 Closure

Test and 1SX037 Stroke Timing, Revision 6B

- CPS 9054.01C002, RCIC 1E51-C001 High Pressure Operability Checks, Revision 3A

- CPS 9054.02, RCIC Valve Operability Checks, Revision 38C

- Work Order 01170713-01, Replace EG-M Box Every 8 yrs, May 6, 2011

- Work Order 01278032-01, Inspect Suppression Pool Suction Check Valve, May 19, 2011

- AR 01211183, WW 1119 SOW Logic Bust With IMD Work

- AR 01211506, 1E51C003: C/O Required For PM, But Not Requested

- AR 01211665, Water from Vent During RCIC SOW

- AR 01212752, WW 1119 RI SOW Unavailable Hours 119% of Scheduled

- ER-AA-600, Risk Management, Revision 6

- ER-AA-600-1012, Risk Management Documentation, Revision 9

- ER-AA-600-1042, On-Line Risk Management, Revision 7

- WC-AA-101, On-Line Work Control Process, Revision 18

- WC-AA-104, Integrated Risk Management, Revision 18

- Clinton Power Station Technical Specifications

- AR 01091836, Plant Risk Yellow Entered When Not Required

1R15 Operability Evaluations

- ER-AA-2009, Managing Gas Accumulation, Revision 1

- Operability Evaluation 384223, 1E21-F303 Leaking By Seat, Revision 0

- Illinois Power Condition Report 1-95-09-025, Check Valve Failure, Revision 0

- Maintenance Request Number D50975, Rework Check Valve to Restore its Function

- Maintenance Request Number D61556, LPCS Test Line Check Valve

- CPS 1401.09F002, Cat A Instrument Failure Checklist, Revision 1

- CPS 9052.01, LPCS/RHR A Pump & LPCS/RHR A Water Leg Pump Operability,

Revision 46a

- CPS 9052.01D001, LPCS/RHR A Pump & LPCS/RHR A Water Leg Pump Operability Data

Sheet, Revision 43d

- CPS 9082.02, Electrical Distribution Verification, Revision 35c

- AR 01204102, Cat A Failure of HPCS Instrument

- AR 01208215, 1E21F303 Abnormal Flow/Indication During LPCS Clearance Hang

- AR 01208296, 1401.09 Enhancements to Cat A Instrument Failure Process

- Work Order 01336205-01, 9052.01 LPCS Pump Operability, July 29, 2010

- M05-1073, Low-Pressure Core Spray (LPCS)(LP), Sheet 1, Revision AG

- M05-1075, Residual Heat Removal (RH), Sheet 1, Revision AW

- M05-1075, Residual Heat Removal (RH), Sheet 4, Revision AF

- Clinton Power Station Technical Specifications

- Clinton Power Station Updated Final Safety Analysis Report, Revision 13

- NRC Regulatory Issue Summary 2005-20, Revision to NRC Inspection Manual Part 9900

Technical Guidance, Operability Determinations & Functionality Assessments for Resolution

of Degraded or Nonconforming Conditions Adverse to Quality or Safety, Revision 1

- EC 384575, High Vibration Levels on 0VC04CB, Revision 0

8 Attachment

- EC 384092, NRC Question on RCS PIV Surveillance Testing, Revision 0

- AR 01219600, Vibration Levels Increased on 0VC04CB

- AR 01202456, NRC Question on RCS PIV Surveillance Testing

- AR 01194749, Division 1 DG Slow Start

- AR 01194803, Transient Test Servers Full - Impact DG Surveillance

- CPS 9080.24, DG 1A Test Mode Override, Load Reject Operability, and Idle Speed

Override, Revision 3a

1R18 Plant Modifications

- AR 01121419, 1DG01KA-A10/A11 DIV I DG Overvoltage Breaker Tripped

- EC 381638, Temporary Modification to Lift Input from A10 Device to A11 Device for the

Division I Diesel Governor, Revision 0

- E02-1DG99, Schematic Diagram Diesel Generator 1A Excitation, Sheet 016, Revision M

- 50.59 Screening Number CL-2010-S-029 for EC #381638, Temporary Modification to Lift

Input from A10 Device to A11 Device for the Division I Diesel Governor, Revision 0

1R19 Post-Maintenance Testing

- EC 379884, Replace Gould Type J13 Auxiliary Relays 1UAY-DG292 and KL With GE

CR120BD Relay in Division 2 EDG Control Panel 1PL12JB, Revision 0

- ECR 394681, DC Operated Type J13 Auxiliary Relay, Revision 0

- CPS 3310.01, Reactor Core Isolation Cooling (RI), Revision 27d

- CPS 9054.01, RCIC System Operability Check, Revision 43

- CPS 9054.01C002, RCIC (1E51-C001) High Pressure Operability Checks, Revision 3a

- CPS 9054.01D002, RCIC (1E51-C001) ) High Pressure Operability Check, Revision 43

- CPS 9054.02, Reactor Core Isolation Cooling Valve Operability Checks Checklist,

Revision 23f

- CPS 9054.02D001, RCIC Valve Operability Data Sheet, Revision 39d

- CPS 9070.01, Control Room HVAC Air Filter Package Operability Test Run, Revision 26d

- CPS 9080.19, DG 1B Overcrank Delay Timer Test, Differential Overcurrent Trip Test, and

Trip Bypass Operability, Revision 0c

- CPS 9080.19D001, DG 1B Overcrank Delay Timer Test Data Sheet, Revision 0

- Work Order 01278032-02, OP PMT for 1E51F030, May 5, 2011

- Work Order 01283985-03, OP PMT for 0VC03CA, April 27, 2011

- Work Order 01294892-01, 1PL12JB: Replace the Division 2 EDG LOCA Bypass Relay

3KL4, March 1, 2011

- Work Order 01294892-03, OPS PMT 9080.19, April 13, 2011

- Work Order 01298883-01, 9054.02D20 OP RCIC Valve Operability (1E51-F079, 81 Only),

May 5, 2011

- Work Order 01363959-02, Generic Replacement of Safety Related Love Controllers,

April 28, 2011

- Work Order 01411430-01, OP 9054.02 RCIC Valve Operability, May 5, 2011

- Work Order 01413537-01, OP 9054.01C002 RCIC 1E51-C001 High Pressure Operability

Check, May 6, 2011

- Work Order 01176252-01, Test Bus 1A1 Main Feed Breaker Protective Relays

- Work Order 00918051-03, Replace Rosemount 1153 Transmitter

- Work Order 01175527-02, Replace and Calibrate Capacity Controller 1TCVP013

- Work Order 01175621-07, PMT for 1TSVP085A & 1TE-VP013

- AR 00985349, 1DG01KA: EDG Div 1 Did Not Go To Full Speed When In Run

- AR 00985660, Found Relay 1UAYDG291 Bad While Troubleshooting 1DG01KA

9 Attachment

- AR 01208618, VC-A SOW PMT Logic Incorrect Delaying Restoration

- AR 01212052, 1E51-F030: Unexpected Torque Readings During Valve Stroke

- AR 01212058, During Performance of 9054.02 Unexpected Values Obtained

- AR 01212267, As Found Torque Is LOOS

- AR 01212373, LL - 9054.02 RCIC Check Valve Operability 1E51-F079

- AR 01212535, 1E51F079: Damaged Set Screw

- AR 01213246, Improved Safety While Testing the 1E51-F030

- M05-1079, RCIC, Sheet 1 Revision AH

- M05-1079, RCIC, Sheet 2 Revision AJ

- Work Order 01405272-02, "0FP03P Outboard Bearing Elevated Temperature"

- Work Order 01404960-01, Horizontal Fire Pump: Perform Operability Test IAW CPS 3822.01

- CPS 3822.06, Operation of the Horizontal Fire Pump, Revision 9

- AR 01203214, Horizontal Fire Pump Packing Hot During Maintenance Run

- AR 01198630, 0FP003 Fire Pump Discharge Packing Leakage Increased

- AR 01198618, 0FP03P (Horizontal FP) INDB/OUTBD Packing Smoking

- AR 01205147, Charger B Voltmeter Failed High 30 VDC (0FP03P)

- AR 01209830, 0FP03P Positive Battery Connector Found Broken on Batter #2

1R22 Surveillance Testing

- CPS 9051.01, HPCS Pump & HPCS Water Leg Pump Operability, Revision 44

- CPS 9051.01D001, HPCS Pump & HPCS Water Leg Pump Operability Data Sheet,

Revision 45

- CPS 9051.02, HPCS Valve Operability Test, Revision 40b

- CPS 9053.04, Residual Heat Removal (RHR) A/B/C Valve Operability Checks, Revision 45b

- CPS 9053.04C002, RHR Loop B Valve Operability, Revision 1b

- CPS 9053.04D002, RHR Loop B Valve Operability Data Sheet, Revision 34b

- CPS 9080.01, Diesel Generator 1A Operability - Manual and Quick Start Operability,

Revision 52.e

- CPS 9866.01, VG/VC [Standby Gas Treatment/Control Room Ventilation] HEPA [High

Efficiency Particulate Air] Filter Leak Test, Revision 26

- Work Order 01403904-01, OP 9051.02 HPCS Valve Operability (Stroke Time), April 18, 2011

- Work Order 01420090-01, Op Perform RHR B Valve Operability Per 9053.04C002, June 13,

2011

- AR 01204162, HPCS Surveillance Enhancement 9051.02 and .05

- Clinton Power Station Technical Specifications

- Clinton Power Station Updated Final Safety Analysis Report, Revision 13

- Clinton Nuclear Power Station Unit 1, Inservice Testing Program Plan - Third Ten Year

Interval, Revision 0

- HU-AA-1212, Technical Task Risk/Rigor Assessment, Pre-job Brief, Independent Third Party

Review, and Post-job Review, Revision 4

- Apparent Cause Evaluation AR 01212825, NRC URI 2011002-04: RCS PIV Leakage

Surveillance Test, June 21, 2011

- CPS 9843.01, ISI [Inservice Inspection] Category A Valve Leak Rate Test, Revision 35

- CL-SURV-10, Risk Analysis for Potentially Deficient Surveillance High to Low Pressure

Interface Valves May Have Been Tested Using Too High a Differential Pressure, Revision 0

- Work Order 1144785-01, MC010-1 LLRT [Local Leak Rate Test] FW [Feedwater] B Line

9861.05D014, January 19, 2010

- Work Order 1144795-01, MC009-1 LLRT FW A Line 9861.05D013, January 17, 2010

- Work Order 1144801-01, 9843.01V003 Category A Valve Leak Rate Test (1E21-F005) LPCS

Injection, January 13, 2010

10 Attachment

- Work Order 1144802-01, 9843.01V003 Category A Valve Leak Rate Test (1E21-F006) LPCS

Injection, January 13, 2010

- Work Order 00790605-01, 1E21-F006 Contingent Rework on LLRT Failure, January 16,

2010

- Work Order 1144820-01, 9843.01V004 Category A Valve Leak Rate Test (1E12-F042C) LPCI

[Low Pressure Coolant Injection] C Drywell Isolation, January 19, 2010

- Work Order 1144817-01, 9843.01V004 Category A Valve Leak Rate Test (1E12-F041C) LPCI

C Test Check Valve, January 19, 2010

- Work Order 1144792-01, 9843.01V018 Category A Valve Leak Rate Test (1E12-F499A/B,

497) RHR Keep Fill, January 19, 2010

- Work Order 1144814-01, 9843.01V001 Category A Valve Leak Rate Test (1E12-F041A) LPCI

A Test Check Valve, January 13, 2010

- Work Order 1144818-01, 9843.01V001 Category A Valve Leak Rate Test (1E12-F042A) LPCI

A Drywell Isolation, January 13, 2010

- Work Order 1144793-01, 9843.01V019 Category A Valve Leak Rate Test (1E12-F495A/B,

496) RHR Keep Fill, January 14, 2010

- Work Order 1144819-01, 9843.01V003 Category A Valve Leak Rate Test (1E12-F042B) LPCI

B Drywell Isolation, January 21, 2010

- Work Order 1144815-01, 9843.01V003 Category A Valve Leak Rate Test (1E12-F041B) LPCI

B Test Check Valve, January 21, 2010

- Work Order 1144828-01, 9843.01V015 Category A Valve Leak Rate Test (1E51-F066) RCIC

Header Spray, January 17, 2010

- Work Order 1144796-01, 9843.01V005 Category A Valve Leak Rate Test (1E22-F004) HPCS

Injection, January 15, 2010

- Work Order 1144797-01, 9843.01V005 Category A Valve Leak Rate Test (1E22-F005) HPCS

Injection, January 15, 2010

- Work Order 1141926-01, 1E22F005 Contingent Repair in Event of LLRT Failure, January 21,

2010

- Work Order 1144810-01, 9843.01V006 Category A Valve Leak Rate Test (1E12-F008) RHR

Shutdown Cooling Suction, January 17, 2010

- Work Order 1144812-01, 9843.01V006 Category A Valve Leak Rate Test (1E12-F009) RHR

Shutdown Cooling Suction, January 17, 2010

- Work Order 1144822-01, 9843.01V009 Category A Valve Leak Rate Test (1E12-F023)

Reactor Pressure Vessel Head Spray, February 1, 2010

- Work Order 1144826-01, 9843.01V009 Category A Valve Leak Rate Test (1E51-F059) RCIC

Test Return to RCIC Storage Tank, February 1, 2010

- AR 01016798, 9843.01D002 Error in Corrected Pressure Calculation

- AR 01198669, Senior Resident NRC Inspector Noted Deficiencies in C1R12 Leak Rate

Testing

- AR 00282084, Discrepancy Between TSSR 3.4.6 and CPS 9843.01

- AR 01202456, NRC Question on RCS PIV Surveillance Testing

- AR 01212825, NRC URI 2011002-04: RCS PIV Leakage Surveillance Test

- AR 01207467, Potential Creep Away From Meeting Regulatory Requirements

- AR 01239007, NRC Identified - VC Flow Issue

2RS3 In-Plant Airborne Radioactivity Control and Mitigation

- RP-AA-302, Determination of Alpha Levels and Monitoring, Revision 3

- RP-AA-440, Respiratory Protection Program, Revision 9

- RP-AA-825, Maintenance, Care and Inspection of Respiratory Protective Equipment,

- Revision 3

11 Attachment

- ProCheck3 Test Results, MSA MMR/Firehawk 4500, Serial Number OY241621, May 6, 2010

- ProCheck3 Test Results, MSA MMR/Firehawk 4500, Serial Number OY241621, June 26,

2009

- ProCheck3 Test Results, MSA MMR/Firehawk 4500, Serial Number QY130249, July 9, 2009

- ProCheck3 Test Results, MSA MMR/Firehawk 4500, Serial Number QY130249,

July 11, 2010

- ProCheck3 Test Results, MSA MMR/Firehawk 4500, Serial Number QY130253, July 9, 2009

- ProCheck3 Test Results, MSA MMR/Firehawk 4500, Serial Number QY130253,

July 11, 2010

- RP-CL-825-101, CPS Maintenance and Care of Respiratory Protective Equipment,

- Revision 33

- System Walkdown for VC (Control Room Ventilation), December 28, 2010

- System Walkdown for VG (Standby Gas Treatment), December 28, 2010

- Work Order Package 01079296 02, 9866.1 Perform HEPA Filter Test on 0VC09SA,

- April 25, 2009

- Work Order Package 00811833 05, Perform HEPA Filter Test on 0VC09SA per CPS 9866.1,

May 2, 2077

- Work Order Package 0109925 05, 9866.1 Perform HEPA Filter Test on 0VC09SB, July 14,

2009

- Work Order Package 00833431 05, Perform HEPA Filter Test on 0VC09SB per CPS 9866.1,

July 17, 2007

- Work Order Package 01136958 05, 9866.1 Perform HEPA Filter Test on 0VG07FB and

0VGG11FB, March 8, 2010

- Work Order Package 01136958 05, 9866.1 Perform HEPA Filter Test on 0VG07FB and

0VGG11FB, March 8, 2010

- Work Order Package 00842268 06, Perform HEPA Filter Test on 0VG07FB and 0VGG11FB

per CPS 9866, November 13, 2007

- Work Order Package 01293106 02, 9866.1 Perform HEPA Filter Test on 0VG07FA and

0VGG11FA, March 1, 2011

- Work Order Package 01089496 025, 9866.1 Perform HEPA Filter Test on 0VG07FA and

0VGG11FA, June 2, 2009

- Work Order Package 01079297 01, 9866.02 Perform Charcoal Adsorber Leak Test

0VC7SA/9SA, April 28, 2009

- Work Order Package 00811832 01, Perform Charcoal Adsorber Leak Test 0VC7SA/9SA per

CPS 9866, May 5, 2007

- Work Order Package 01099926 01, 9866.02 Perform Charcoal Adsorber Leak Test

0VC7SB/9SB, July 7, 2009

- Work Order Package 01265331 02, 9866.02 Perform Charcoal Adsorber Leak Test

0VG08FA, March 1, 2011

- Work Order Package 01089817 02, 9866.02 Perform Charcoal Adsorber Leak Test

0VG08FA, March 2, 2009

- Work Order Package 01136959 05, 9866.02 Perform Charcoal Adsorber Leak Test

0VG08FB, March 18, 2010

- Quarterly Service Air and Self Contained Breathing Apparatus, December 17, 2009

- Quarterly Service Air and Self Contained Breathing Apparatus, March 12, 2010

- Quarterly Service Air and Self Contained Breathing Apparatus, June 25, 2010

- Quarterly Service Air and Self Contained Breathing Apparatus, July 30, 2010

- Quarterly Service Air and Self Contained Breathing Apparatus, September 17, 2010

- Quarterly Service Air and Self Contained Breathing Apparatus, February 23, 2011

- AR 01214577, Mask in Premaire Unit Found with Bad Exhalation Diaphragm, May 11, 2011

- AR 01215101, Storage of Licensed Operator Respirator Spectacle Kits, May 12, 2011

12 Attachment

- AR 01215230, Review Need for Validation of Respirator Spectacle Kits, May 12, 2011

- AR 01215184, SCBA HUD Batteries are not the Recommended Batteries, May 12, 2011

- AR 0121513, SCBA Face piece Drying Gap, May 12, 2011

- MSA MMR Air Mask with Firehawk Regulator, Operating and Instruction Manual, TAL 406

(L), Revision 12

2RS4 Occupational Dose Assessment

- NUPIC Audit SA10-017, Mirion Technologies (GDS) Inc., January 3, 2011

- RP-AA-210-2001, Ability to Wear the Thermoluminescent Dosimeter (TLD) Under Protective

Clothing, Revision 0

- RP-AA-11, External Dose Control Program, Revision 0

- RP-AA-12, Internal Dose Control Program Description, Revision 1

- RP-AA-203; Exposure Control and Authorization, Revision 3

- RP-AA-203-1001, Personnel Exposure, Revision 6

- RP-AA-210, Dosimetry Issue, Usage, and Control, Revision 20

- RP-AA-210-1001, Dosimetry Logs and Forms, Revision 5

- RP-AA-214, Area TLD Surveillance, Revision 3

- RP-AA-220 Bioassay Program, Revision 7

- RP-AA-221, Whole Body Data Review, Revision 1

- RP-AA-222, Methods for Estimating Internal Exposure from In Vivo and In Vitro Bioassay

Data, Revision 3

- RP-AA-230, Operation of the Canberra FASTSCAN Whole Body Counter, Revision 0

- RP-AA-250, External Dose Assessments from Contamination, Revision 5

- Calibration of the Canberra FASTSCAN WBC System at the Clinton Power Station, 2/24/2011

- Audit SA 10-017; QAD2011001, Joint Audit of Mirion Technologies (GDS) Inc., January 3,

2011

- Audit SR 2008-001, Joint Audit of Global Dosimetry Solutions, January 10, 2008

- FASA, Occupational Dose Assessment & In Plant Airborne Radioactivity Control & Mitigation,

Assignment 1056527-03, February 1, 2011

- RP-AA-270, Prenatal Radiation Exposure, Revision 6

- AR 01215225, Passport Expiration Date of DPW Needs Improvement, May 12, 2011

- AR 01215180, RP Procedure Enhancement to Clarify Attachment Use, May 12, 2011

4OA1 Performance Indicator Verification

- AR 01113608, Div 2 EDG Quick Start Time > 9080.02 Step 9.1.6 Criteria

- AR 01187358, Change 9080.26 to Eliminate an Unnecessary Engine Start

- AR 01194749, Division 1 Slow Start Time

- AR 01214578, 1DG01KB: D2 DG Tripped During 9080.02

- CPS 9000.01D001, Control Room Surveillance Log - Mode 1, 2, 3 Data Sheet, Revision 52e

- LS-AA-2200, Mitigating System Performance Index Data Acquisition & Reporting, Revision 3

- LS-AA-2001, Collecting and Reporting of NRC Performance Indicator Data, Revision 14

- Nuclear Energy Institute 99-02, Regulatory Assessment Performance Indicator Guideline,

Revision 6

- RM Document Number CL-MSPI-01, Clinton MSPI Basis Document, Revision 5

- MSPI Derivation Reports, Period March 2011, for Emergency AC Power System

- Nuclear Energy Institute 99-02, Regulatory Assessment Performance Indicator Guideline,

Revision 6

13 Attachment

4OA2 Identification and Resolution of Problems

- ANSI/ANS 56.8-2002, "Containment System Leakage Testing Requirements"

- NEI 94-01, "Industry Guideline for Implementing Performance-based Option of 10 CFR Part

50, Appendix J"

- NRC Information Notice 85-71, Containment Integrated Leak Rate Tests

- Regulatory Guide 1.163, "Performance-Based Containment Leak-Test Program"

- CPS 1305.01, Primary Containment Leakage Rate Testing Program, Revision 10c

- CPS 1305.01F001, Type 'B' Local Leak Rate Summary Sheet, Revision 2

- CPS 9861.04, MSIV Local Leak Rate Test (MC-5,6,7,8), Revision 26

- CPS 9861.04D002, MSIV B Local Leak Rate Test Data Sheet (1MC-8), Revision 25d

- Work Order 01128244, MC008 LLRT Requirements (MSIV - B) and PIT 1E32-F001E,

January 20, 2010

- Operational and Technical Decision Making (OTDM) #1229710, Through Wall Steam Leak on

1MS13AA-2

- RCR 1021241, Late Identification of Work Scope for 1B21F022C, Inboard Main Steam Line C

Isolation Valve

- EACE 1017464, Investigate Failure of 'B' MSIVs

- AR 01017464, 1B21F028A: 9861.04 LLRT on MSL A, B, and C Test Failure

- AR 01059673, NOS ID MSIV As-Found Results Re-Evaluate Reportability

- AR 01224527, NRC PI&R: As-Found LRT For Each MSIV Not Performed In C1R12

- AR 01228126, Heater Bay Hotter Than Expected

- AR 01229320, Steam Leak Identified On 1ES001B

- AR 01229325, 1WO03SL - Water Dripping Near 1FW01AA 6A HP Heater

- AR 01229569, 1ES001A Has Small Packing Leak

- AR 01229710, Through Wall Steam Leak On 1MS13AA-2

- AR 01231642, Need Contingent Actions For High Heater Bay Temperatures

- AR 01232761, Water Flow Check For Turbine Building Area Coolers

- AR 01233539, Replace 2 Inch Pipe 1MS13AB Downstream Of Valve 1B21CA6

- AR 01233540, Replace 2 Inch Pipe 1MS13AC Downstream of Valve 1B21CA5

4OA3 Followup of Events and Notices of Enforcement Discretion

- LER 05000461/2008-001-02, "Reactor Recirculation Pump Trip Initiates Automatic Scram on

High RPV Water Level," Supplement 2

- LER 05000461/2009-005-01, "Manual Scram on High Water Level Due to Reactor

Recirculation Pump Trip," Supplement 1

4OA5 Other Activities

- 0000-0088-8669-R0, BWR Owners Group Technical Report Effects of Voiding in ECCS

Drywell Injection Piping, September 2008

- 0000-0088-8669-R0, BWR Owners Group Technical Report; Effects of Voiding in ECCS

Drywell Injection Piping, September 2008

- 3C10-0175-001, Design and Analysis of Clinton Containment Spray System, Revision 3A

- AR 00807753, NRC GL 08-01 Inspection Results At Pipe 1RH50AB

- AR 00812163, NRC GL 2008-01 Inspection Results at Pipe 1RH

- AR 01212387, NRC GL 2008-01 Lack of Gas Management RHR Discharge Piping Void

- AR00802940, GL 08-01 Inspection Results at 1E12F037A, August 1, 2008

- AR00807753, GL 08-01 Inspection Results at 1RH50AB, August 15, 2008

- AR00812163, GL 08-01 Inspection Results at 1RH03AA, August 28, 2008

14 Attachment

- AR00814512, GL 08-01 Inspection Results at 1RH117A, September 5, 2008

- AR01022886, RHR C Pump Suction Voiding, January 28, 2010

- AR01173402, FASA Eval Adding Time Duration to Venting Act, February 10, 2011

- AR01195401, GL 2008-01 Inspection Findings at Byron/Braidwood, March 31, 2011

- AR01195408, GL 2008-01 Inspection Findings at Byron/Braidwood, March 31, 2011

- AR01197314, GL 2008-01 Inspection Findings at Byron/Braidwood, April 4, 2011

- AR01212387, Lack of Gas Management RHR Discharge Piping Void, May 5, 2011

- ATI-992573-07, NRC IN 2010-11 Voiding in RHR Piping

- CPS 3309.01, High Pressure Core Spray (HPCS), Revision 16a

- CPS 3312.01, Residual Heat Removal, Revision 38c

- CPS 3312.03, RHR - Shutdown Cooling (SDC) and Fuel Pool Cooling and Assist (FPC&A),

Revision 6c

- CPS 9051.01, HPCS Pump and HPCS Water Leg Pump Operability, Revision 44a

- CPS 9051.05, HPCS Discharge Header Filled and Flow Path Verification, Revision 27e

- CPS 9053.01, RHR B/RHR C Discharge Header Filled and Flow Path Verification,

Revision 28F

- EC 371529, Generic Letter 2008-01 HPCS Evaluation, Revision 1

- EC 371531, GL 2008-01 System Evaluation Template, Exelon Specific, Clinton Power Station

- RHR Evaluation, Revision 1

- EC 371609, Ultra Sonic Inspection Criteria: Division 1 ECCS: RHR A/LPCS, Revision 1

- EC 371659, Generic Letter 2008-01 Air Intrusion in ECCS Systems Ultrasonic Inspection

Criteria Division 2 ECCS: RHR-B/RHR-C; Revision 1,

- EC 371983, Installation of High Point vent on Line 1RH50AB-10 Cancel to EC373186 and

Calc IP-M-0777, August 16, 2010

- EC 373186, Piping Air Pocket acceptance (NRC GL 2008-01), Valve Bonnet and Known

Pockets, Revision 0

- EC-371560, HPCS Vent Modification, Revision 0

- EC-371660, Generic Letter 2008-01: Air Intrusion in ECCS Systems Ultra-sonic Inspection

Criteria: Division 3 ECCS: HPCS, Revision 1

- EC-380824, Generic Letter 2008-01 System Periodic UT Frequency Evaluation Clinton Power

Station - RHR, LPCS and HPCS; Revision 0

- ER-AA-2009, Managing Gas Accumulation, Revision 1

- ER-AA-335-007, Ultrasonic Inspection for Determination of Sedimentation in Piping Systems

or Components and Fluid Level Measurements, Revision 3

- FAI/08-70, Gas Void Pressure Pulsations Program, Revision 0

- HP-1, High Pressure Core Spray Isometric Drawing;Revision 7U

- HP-2, High Pressure Core Spray Isometric Drawing; Revision 10L

- HP-3, High Pressure Core Spray Isometric Drawing; Revision 6A

- HP-4, High Pressure Core Spray Isometric Drawing; Revision 7E

- HP-5, High Pressure Core Spray Isometric Drawing; Revision 9N

- HP-6, High Pressure Core Spray Isometric Drawing; Revision 6R

- M05-1074, P&ID High Pressure Core Spray; Revision AH

- M05-1075-001, P& ID Residual Heat Removal (RH), Revision AW

- M05-1075-002, P& ID Residual Heat Removal (RH), Revision AM

- M05-1075-003, P& ID Residual Heat Removal (RH), Revision AG

- Operability Evaluation 812163-02, Residual Heat Removal System, January 13, 2009

- Power Point Presentation on Training for GL 2008-01

- RH-09, System: Residual Heat Removal Isometric Drawing, Revision 7A

- RH-11, System: Residual Heat Removal Isometric Drawing, Revision 5M

- RH-14, System: Residual Heat Removal Isometric Drawing, Revision 12M

- RH-17, System: Residual Heat Removal Isometric Drawing, Revision 8H

15 Attachment

- RH-21, System: Residual Heat Removal Isometric Drawing, Revision 11L

- RS-08-131, Nine-Month Response to Generic Letter 2008-01, October 14, 2008

- RS-09-173, Response to Request for Additional Information Regarding Generic Letter 2008-01, December 15, 2009

- WO01359924, UT Testing to Check for Accumulated Air - HPCS, October 18, 2008

- WO01379900, UT Testing to Check for Accumulated Air - HPCS, January 17, 2011

- AR01206227, Missed Impacts to RCIC Cooling Load Calculations, April 22, 2011

- AR01208619, 12-Minutes Basis in Procedure - Injection Piping Fill Time, April 27, 2011

- AR01212387, NRC GL 2008-01 Lack of Gas Management RHR Discharge Piping Void,

May 5, 2011

- AR01205245, SX Rooms Watertight Doors SD1-11 and SD1-12 are Found Open,

April 20, 2011

- AR01205404, Document Update Missed in EC, April 20, 2011

- AR01209715, NRC IN 2010-11 Response, April 29, 2011

16 Attachment

LIST OF ACRONYMS USED

AC Alternating Current

ADAMS Agency-wide Documents and Management System

AR Action Request

BI Barrier Integrity

CFM Cubic Feet Per Minute

CFR Code of Federal Regulations

CNO Chief Nuclear Officer

DG Diesel Generator

DHR Decay Heat Removal

ECCS Emergency Core Cooling System

°F Degrees Fahrenheit

FIN Finding

GL Generic Letter

GPM Gallons Per Minute

HEPA High Efficiency Particulate Air

HPCS High Pressure Core Spray

HVAC Heating Ventilation and Air Conditioning

IE Initiating Events

IMC Inspection Manual Chapter

IP Inspection Procedure

ISI Inservice Inspection

LER Licensee Event Report

LLRT Local Leak Rate Test

LOCA Loss-of-Coolant-Accident

LPCS Low Pressure Core Spray

MS Mitigating Systems

MSL Main Steam Line

MSPI Mitigating Systems Performance Index

NCV Non-Cited Violation

NEI Nuclear Energy Institute

NIOSH National Institute for Occupational Safety and Health

NRC U.S. Nuclear Regulatory Commission

NRR Office of Nuclear Reactor Regulation

P&ID Piping and Instrumentation Diagram

PARS Publicly Available Records System

% Percent

PIV Pressure Isolation Valve

PMT Post-Maintenance Test

PSIG Pounds Per Square Inch Gauge

RCIC Reactor Core Isolation Cooling

RCS Reactor Coolant System

RHR Residual Heat Removal

SAMG Severe Accident Management Guidelines

SBO Station Blackout

SCBA Self Contained Breathing Apparatus

SDP Significant Determination Process

SSC Structures, System, and Component

SX Shutdown Service Water

TEDE Total Effective Dose Equivalent

17 Attachment

TI Temporary Instruction

TR Topical Report

TS Technical Specification

TSO Transmission System Operator

TSSR Technical Specification Surveillance Requirement

TSTF Technical Specification Task Force

UHS Ultimate Heat Sink

UFSAR Updated Final Safety Analysis Report

URI Unresolved Item

VC Control Room Ventilation

VG Standby Gas Treatment

Work Order Work Order

WR Work Request 18 Attachment

M. Pacilio -2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter,

its enclosure, and your response (if any) will be available electronically for public inspection in

the NRC Public Document Room or from the Publicly Available Records System (PARS)

component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Website

at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Mark A. Ring, Chief

Branch 1

Division of Reactor Projects

Docket No. 50-461

License No. NPF-62

Enclosure: Inspection Report 05000461/2011-003

w/Attachment: Supplemental Information

cc w/encl: Distribution via ListServ

DISTRIBUTION:

See next page

DOCUMENT NAME: G:\DRPIII\1-Secy\1-Work In Progress\CLIN 2011 003.docx

Publicly Available Non-Publicly Available Sensitive Non-Sensitive

To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl

"E" = Copy with attach/encl "N" = No copy

OFFICE Clinton RIO RIII E RIII RIII

NAME MRing for BKemker MRing:cs

DATE 07/29/11 07/29/11

OFFICIAL RECORD COPY

Letter to M. Pacilio from M. Ring dated July 29, 2011

SUBJECT: CLINTON POWER STATION, NRC INTEGRATED INSPECTION REPORT

05000461/2011-003

DISTRIBUTION:

Daniel Merzke

RidsNrrDorlLpl3-2 Resource

RidsNrrPMClinton Resource

RidsNrrDirsIrib Resource

Cynthia Pederson

Steven Orth

Jared Heck

Allan Barker

Carole Ariano

Linda Linn

DRSIII

DRPIII

Patricia Buckley

Tammy Tomczak

ROPreports Resource