IR 05000461/2021012

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Biennial Problem Identification and Resolution Inspection Report 05000461/2021012
ML21179C287
Person / Time
Site: Clinton Constellation icon.png
Issue date: 06/28/2021
From: Kenneth Riemer
Division Reactor Projects III
To: Rhoades D
Exelon Generation Co, Exelon Nuclear
References
EPID I-2021-012-0015 IR 2021012
Download: ML21179C287 (16)


Text

June 28, 2021

SUBJECT:

CLINTON POWER STATION - BIENNIAL PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000461/2021012

Dear Mr. Rhoades:

On May 21, 2021, the U.S. Nuclear Regulatory Commission (NRC) completed a problem identification and resolution inspection at your Clinton Power Station and discussed the results of this inspection with Mr. T. Chalmers, Site Vice President, and other members of your staff.

The results of this inspection are documented in the enclosed report.

The NRC inspection team reviewed the stations corrective action program and the stations implementation of the program to evaluate its effectiveness in identifying, prioritizing, evaluating, and correcting problems, and to confirm that the station was complying with NRC regulations and licensee standards for corrective action programs. Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

The team also evaluated the stations processes for use of industry and NRC operating experience information and the effectiveness of the stations audits and self-assessments.

Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

Finally, the team reviewed the stations programs to establish and maintain a safety-conscious work environment and interviewed station personnel to evaluate the effectiveness of these programs. Based on the teams observations and the results of these interviews, the team found no evidence of challenges to your organizations safety-conscious work environment.

Your employees appeared willing to raise nuclear safety concerns through at least one of the several means available.

No findings or violations of more than minor significance were identified during this inspection. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Kenneth R. Riemer, Chief Branch 1 Division of Reactor Projects

Docket No. 05000461 License No. NPF-62

Enclosure:

As stated

Inspection Report

Docket Number:

05000461

License Number:

NPF-62

Report Number:

05000461/2021012

Enterprise Identifier: I-2021-012-0015

Licensee:

Exelon Generation Company, LLC

Facility:

Clinton Power Station

Location:

Clinton, IL

Inspection Dates:

May 03, 2021 to May 21, 2021

Inspectors:

J. Kutlesa, Physical Security Inspector

V. Meghani, Reactor Inspector

R. Ng, Project Engineer

D. Sargis, Resident Inspector

Approved By:

Kenneth R. Riemer, Chief

Branch 1

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a biennial problem identification and resolution inspection at Clinton Power Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

None.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

Starting on March 20, 2020, in response to the National Emergency declared by the President of the United States on the public health risks of the Coronavirus Disease (COVID-19), regional inspectors were directed to begin telework. During this time regional baseline inspections were evaluated to determine if all or portions of the objectives and requirements stated in the IP could be performed remotely. In some cases, portions of an IP were completed remotely and on-site.

The inspection documented below was determined that the objectives and requirements stated in the IP could be completed remotely.

OTHER ACTIVITIES - BASELINE

71152B - Problem Identification and Resolution Biennial Team Inspection (IP Section 02.04)

(1) The inspectors performed a biennial assessment of the licensees corrective action program, use of operating experience, self-assessments and audits, and safety conscious work environment.
  • Corrective Action Program Effectiveness: The inspectors assessed the corrective action programs effectiveness in identifying, prioritizing, evaluating, and correcting problems. The inspectors also conducted a 5-year review on shutdown service water piping leakage and FLEX related issues. Note that the inspectors did not review the corrective actions related to a White NOV in the Security cornerstone since the Inspection Procedure 95001 Supplemental Inspection has not been completed.
  • Operating Experience, Self-Assessments and Audits: The inspectors assessed the effectiveness of the stations processes for use of operating experience, audits, and self-assessments.
  • Safety Conscious Work Environment: The inspectors assessed the effectiveness of the stations programs to establish and maintain a safety-conscious work environment.

INSPECTION RESULTS

Assessment 71152B Based on the samples reviewed, the team concluded that the licensee's implementation of the Corrective Action Program was generally effective and supported nuclear safety.

Effectiveness of Problem Identification:

Based on the samples reviewed, the team concluded that the licensee continued to identify issues at a low threshold and appropriately entered these issues into the Corrective Action Program. The team determined that the licensee usually entered problems into the Corrective Action Program completely and accurately. However, the team identified a condition adverse to quality that should have been entered into the Corrective Action Program for resolution. Additional details of this issue are discussed in the Minor Violation section of this report.

The team also noted that some deficiencies were identified by external organizations, including the NRC, that had not been previously identified by licensee staff and were subsequently entered into the Corrective Action Program. In addition, the licensee also utilized a number of Corrective Action Program support processes to identify problems, including the self-assessment and audit process and the Operating Experience Program. For example, the licensee performed department self-assessments and quality assurance audits to identify issues in station processes. Similarly, the licensee screened issues from both NRC and industry operating experience and entered them into the Corrective Action Program when they were applicable to the station.

The team determined that the licensee was generally effective at trending low-level issues and taking appropriate corrective actions to prevent more significant problems from developing. In addition, the licensee used the Corrective Action Program to document instances in which previous corrective actions were ineffective or were inappropriately closed.

The team performed a 5-year review of the shutdown service water piping leakage issues.

As part of this review, the team interviewed the system engineer, reviewed the plant health report, and reviewed selected corrective actions and condition evaluation documents. In addition, the team performed a partial system walkdown to assess the material condition of the system piping and surrounding areas. The team concluded that the shutdown service water system piping degradation and leakage concerns were identified and entered into the Corrective Action Program at a low threshold and were resolved in a timely manner commensurate with their safety significance. For the areas walked down, the team did not identify any additional issues.

Effectiveness of Prioritization and Evaluation of Issues:

Based on the samples reviewed, the team determined that licensee performance was generally effective at prioritizing and evaluating issues commensurate with the safety significance of the identified problem. The Ownership Screening Committee and the Management Review Committee meetings were generally thorough and intrusive in reviewing issues and prioritizing actions. In addition, the team observed a productive dialogue between the members of these committees and the members challenged each other when dispositioning issues.

In general, once a degraded or non-conforming condition was identified, the Corrective Action Program directed that an equipment operability or functionality review be performed. As a result, the majority of the samples reviewed were evaluated in a timely manner.

Effectiveness of Corrective Actions:

Based on the samples reviewed, the team determined that the licensee was generally effective in corrective action implementation. In general, corrective actions for deficiencies that were safety significant were implemented in a timely manner. Problems identified using a root cause or other cause methodologies were resolved in accordance with Corrective Action Program requirements. The corrective actions assignments that were sampled by the team for selected NRC documented violations and for licensee event reports (LERs) were generally effective and timely.

The team performed a 5-year review of the stations diverse and flexible coping strategies (FLEX). As part of this review, the team reviewed corrective action documents, the plant health report, the licensee's responses to various industry operating experiences and previously identified NRC findings related to FLEX. In addition, the team performed a partial system walkdown to assess the material condition and proper storage and staging of FLEX equipment. The team concluded that FLEX system deficiencies were identified and entered into the Corrective Action Program at a low threshold and were generally resolved in a timely manner commensurate with their safety significance. The inspectors did not identify any violations of NRC requirements.

Assessment 71152B Based on the samples reviewed, the team determined that licensee's performance in the use of operating experience was generally effective. The licensee's corporate office screened industry and NRC operating experience information for applicability to Clinton Power Station.

Based on these initial screenings, the licensee-initiated actions in the Corrective Action Program to fully evaluate the impact, if any, to the station. When applicable, actions were developed and implemented to prevent similar issues from occurring. Operating experience lessons learned were communicated and incorporated into plant operations. The team observed the information being used in daily activities, such as pre-job briefs, as well as issue reviews and investigations.

Assessment 71152B Based on the samples reviewed, the team determined that the licensee's performance of self-assessments and audits was generally effective. The licensee performed department self-assessments and quality assurance audits throughout the organization on a periodic basis. These self-assessments and audits were generally effective at identifying issues and enhancement opportunities at an appropriate threshold. The self-assessments and audits reviewed by the team identified issues that were not previously known, including issues within the Corrective Action Program itself. Nuclear Oversight (NOS) identified deficiencies with the licensee's processes and those issues were addressed by the station through the Corrective Action Program.

Assessment 71152B Based on a review of documents and interviews with licensee staff, the team did not identify any impediment to the establishment of a safety conscious work environment. The team reviewed the results from the 2020 Safety Culture Assessment, the culture survey from first quarter of 2021 performed by the licensee, and the Nuclear Safety Culture Monitoring Panel meeting minutes. The team also conducted one-on-one interviews with 20 licensee staff concerning the effectiveness of the Corrective Action Program, the ability to raise issues, and the freedom from potential retaliation for raising issues.

In general, the licensee's staff was aware of and familiar with the Corrective Action Program and other processes, such as the Employee Concerns Program, to raise nuclear safety concerns. Licensee staff indicated they could raise safety concerns without a fear of retaliation. Through the interviews and document reviews, the team was not provided or identified any examples of retaliation for raising nuclear safety concerns. The staff interviewed believed that operational issues and issues with high safety significance were being appropriately addressed in a timely manner.

Minor Violation 71152B Minor Violation: In 2019, the licensee added a section in Procedure 3309.01, High Pressure Core Spray (HPCS), to maintain HPCS availability using the recycle condensate system should the waterleg pump not be available to keep the system full of water. This portion of the procedure would direct the operators to open the isolation valves between the two systems and use the recycle condensate system to fill and vent the HPCS system. In June of 2019, an operator identified the potential of over-pressurizing the recycle condensate system if HPCS auto starts during this activity because the low pressure recycle condensate system would be opened to the high-pressure HCPS system. The issue was screened as a non-corrective action program (NCAP) item and not resolved or evaluated until the inspectors reviewed this issue during this inspection.

When questioned by the inspectors about the consequences of the over-pressurization, the licensee stated that it could cause piping failure or leakage in the recycle condensate system.

In addition, it would also divert the needed HPCS injection to the recycle condensate system.

The licensee did not have a formal engineering evaluation of the potential consequences.

The licensee agreed that this issue is a condition adverse to quality and should have screened as a corrective action program item. The licensee has issued a Daily Order to suspend the use of this section of the procedure.

Since the revision of the procedure in 2019, the licensee has not executed this section of the procedure. Given the isolation valves between the two systems was a safety related class 2 piping and an operator would be present and in communication with the main control room during this activity, the inspectors determined that the operator could close the isolation valves promptly even if HPCS auto starts and damage occurs in the recycle condensate system.

The inspectors determined that the failure to identify a condition adverse to quality and promptly correct the condition is a performance deficiency and a violation of 10 CFR 50, Appendix B, Criterion XVI, "Corrective Actions."

Screening: The inspectors determined the performance deficiency was minor. The inspectors determined that this issue is minor because this issue is similar to IMC 0612, Appendix E, Example 4.g. This performance deficiencies did not adversely affect the mitigating systems cornerstone objective because this is a failure to identify the issue and implement a corrective action that had little safety impact. This activity has never been performed since the procedure revision and the isolation valves were accessible and could be closed to recover the HPCS system by the operator standing by in the area during the activity.

Enforcement:

This failure to comply with 10 CFR 50, Appendix B, Criterion V, "Corrective Actions," constitutes a minor violation that is not subject to enforcement action in accordance with the NRCs Enforcement Policy. The licensee issued a Daily Order to prevent the utilization of that section of the procedure and entered the issue in their CAP as AR

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On May 21, 2021, the inspectors presented the biennial problem identification and resolution inspection results to Mr. T. Chalmers, Site Vice President, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71152B

Corrective Action

Documents

AR 1296821

3514.01C012 480V Unit Sub 1D Bus Outage Checklist

Impacts

2/01/2011

AR 1329147

1PL12JA-A1: Re-Evaluate EDG Voltage Regulator R3

Replacement

2/20/2012

AR 1390648

Protective Relay Tolerances Require Fleet Review

07/19/2012

AR 1403682

Received Unexpected Annunciator 5050-5H, Trouble SGTS

Elect

08/22/2012

AR 1460640

NRC Question MRFR for 1VX06CA / 1SX024A,

AR 1383458-03

01/09/2013

AR 1474231

Maintenance ATV-Systematic Approach to Training - 2019

01/01/2020

AR 1483230

Enhancement for Protective Relay Calculations

03/04/2013

AR 1594407

Automatic Trip of Breaker 1PA07EJ

2/09/2013

AR 1627756

1DC05E Has More Than Half of Cells Weeping

2/28/2014

AR 2381871

Failure of the Outer/Upper Motor Bearing for 1SX01PC

09/16/2014

AR 2556763

Enhancement Maintaining Valid Control Rod Position

09/17/2015

AR 2560629

SX DIV 1 Supply Header Low Point Drain Leak

09/25/2015

AR 2598038

UT Results On 1sx01ab-30" Are Near Code Allowable

Min-Wall

2/09/2015

AR 2600682

UT Results On 1SX203AB-2"

2/15/2015

AR 2610350

RWCU Isolation Due to Failed Temperature Instrument

01/10/2016

AR 2621780

1FC004B Failed Stroke Time

01/04/2016

AR 2655457

(2016 CDBI FASA) Calc 19-AJ-18 Weakness

04/14/2016

AR 2695275

NRC Question on Operability of Div 1 SX During

Maintenance

07/21/2016

AR 2733400

WO Required for Inspection of Weld Overlay on SX Piping

10/27/2016

AR 2733400

WO Required for Inspection of Weld Overlay on SX Piping

10/27/2016

AR 2742442

CDBI: Inappropriate Calculation Method for CR Habitability

11/17/2016

AR 3944082

NRC NCV 2016003-04 Fail to Prevent Recurrence of a

SCAQ

11/22/2016

AR 3969239

NRC NCV 2016009-02 SFP Temp and Level Not in MRULE

2/01/2017

AR 3987864

Procedure Revisions for EC 618355, 1CO04J

03/21/2017

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

AR 4001089

NRC Cited Violation for Design Control

04/21/2017

AR 4051565

Error in Calc 3C10-0485-001 Associated with Flood Level

09/13/2017

AR 4051565

Error in Calc 3C10-0485-001 Associated with Flood Level

09/13/2017

AR 4105738

1SX019A Has Valve Erosion at The Lower Disc Pin Area

2/19/2018

AR 4110203

Root Cause for NRC Div 3 SX Pump White Finding

03/01/2018

AR 4125840

11AA: 2018 UT Results Lower Than Expected

04/12/2018

AR 4125840

1SX111AA: 2018 UT Results Lower Than Expected

04/12/2018

AR 4158854

1SXB5BA: 2018 UT Results Lower Than Expected

07/25/2018

AR 4166869

ECAPE 4116223 Extent of Condition Work Orders Cancelled

08/24/2018

AR 4177094

NRC INFO NOTICE 2018 Kobe Steel QA Falsification

09/26/2018

AR 4185385

Mechanical Snubbers Removed Without EQ Review

10/19/2018

AR 4220546

EP OE: Offsite Notification Due to Inadvertent Siren Activate

2/15/2019

AR 4220600

NOS: EP ID: Evacuation Route Signs are Illegible

2/15/2019

AR 4222006

EP ID: 2019 NRC Pre-Exercise - OSC Performance

2/20/2019

AR 4230952

NRC IN 2019-01: Inadequate Evaluation of Temp Alterations

03/19/2019

AR 4248447

EP ID: RSCL Phone Line INOP

05/13/2019

AR 4250932

1AP07EK Main Feed Breaker Failed to Close During Bus

Shift

05/22/2019

AR 4250998

NRC ID: Paragon Risk Incorrect

05/22/2019

AR 4251273

EP ID: ERO Focus Area Drill Rescheduled

05/23/2019

AR 4251489

Entered 4002.01, Abnormal RPV Level/Loss of FW at Power

05/24/2019

AR 4255647

PCRA 3209.01 HPCS CY Float Start

06/10/2019

AR 4258645

2SXA9AA: UT Results Lower Than Acceptance Criteria

06/21/2019

AR 4258645

2SXA9AA: UT Results Lower Than Acceptance Criteria

06/21/2019

AR 4260500

SEC ID: Complete Loss of Power to CAS and SAS

06/28/2019

AR 4262593

EP ID: Trend IR: Multiple CPS Siren Failures

07/08/2019

AR 4263520

Flex Diesel Generator Phase Rotation

07/11/2019

AR 4269131

NRC NCV 2019040-01: Fail to Complete EFR for CAPR

08/02/2019

AR 4269353

Root Cause Investigation Report; TDRFP B Turbine LVDT

Failure Results in an Automatic RPS SCRAM on RPV

Level 3

09/11/2019

AR 4272994

NRC FIN 2019002-01 Fail Prop Eval Plant Risk

08/19/2019

AR 4277173

NRC IN 2019-05: Overpressurization of Alpha Sources

09/06/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

AR 4278245

Arc Flash Event

09/11/2019

AR 4280147

TDRFP B Scram Lessons Learned: LVDT/Torque Arm

Strategies

09/18/2019

AR 4284526

EOID SRV 51B Actuates Instead of 41B

10/02/2019

AR 4286641

1E22F015 HPCS Suction Valve Did Not Open During Valve

Stroke

10/10/2019

AR 4288235

NRC IN 2019-08 OPEX Regarding FAC Causing RX Scrams

10/19/2018

AR 4297570

Root Cause Report: FLEX Diesel Generator 1FX01KA

Incorrect Phase Rotation

11/15/2019

AR 4301533

CAPE: Fire Protection System and Program Health

2/04/2019

AR 4307907

SLC Pressure Regulator 1C41-F351 Reads Above Full Scale

01/03/2020

AR 4311763

Contraband Introduced into the Protected Area (PA)

03/12/2020

AR 4312418

EP-IEMA EMNET Phones Inoperable

01/24/2020

AR 4329201

CAPE: Entered Loss of Feedwater Heating 4A Heater

Restoration

03/24/2020

AR 4340981

CAPE: Personnel Entered Precautionary Posted HRA

Without HRA Brief

05/04/2020

AR 4346309

NRC FIN 2020001-01 FLEX Diesel Generator Phase

Rotation

05/28/2020

AR 4352937

CAPE: FLEX Diesel Generator Breaker Settings

06/26/2020

AR 4364203

1SX29BB-3", Div II SX Strainer Backwash Pipe Replacement 08/19/2020

AR 4365604

EP: Clinton 2020 Off-Year Exercise - TSC Issues

08/26/2020

AR 4369686

NRC IN 2020-02 - Flex Diesel Operational Challenges

09/16/2020

AR 4370305

NRC IN 2020-01 - Electr. Equip. Issues After COVID

Cleaning

09/18/2020

AR 4374683

Need Procedure Revision on 9433.23 ECCS HPCS Pump

E22-N051

10/06/2020

AR 4383175

NRC IN 2020-03 Recall of Edwards 135 Degree Heat

Detectors

11/09/2020

AR 4384779

CAPE: 0VC21YB 0VC24YB & 0VC27YB Lost Power

11/16/2020

AR 4390355

Sec AA/FFD Clinton Security Training Inst CG Requirements

Expired

2/15/2020

AR 4391803

NRC IN 2020-04 - FP Mn Yard Buried Cast Iron Piping

Failures

2/23/2020

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

AR 4401345

NRC ID: Observation on 30-Day Observations of Remote

Workers

2/09/2021

AR 4404476

NRC Green FIN 2020004-01 FLEX DG Settings for Output

Breakers

2/24/2021

AR 4408095

0WM118B Through Wall Leak

03/11/2021

AR 455060455060Closure of B.5.B Phase 1 NRC Issues

2/17/2016

AR 916815916815RCIC Tripped During Startup

05/07/2009

Corrective Action

Documents

Resulting from

Inspection

AR 4421725

PCRA PI-AA-125-1003

05/05/2021

AR 4421740

PCRA for PI-AA-125-1001

05/05/2021

AR 4422020

PI&R 2021: RCR 4269353 Missing CA for Contributing

Cause

05/06/2021

AR 4422255

WO for Digital Feedwater Testing Not Supervisory Reviewed

06/06/2021

AR 4422839

Response to CA 4284526-29 Not Robust

05/11/2021

AR 4423155

Lesson Learned IR 4280147 Action Canceled in Error

05/12/2021

AR 4424142

NRC ID: Operations S.O. for DHP Brkr List is Not Current

05/17/2021

AR 4424391

Response to Action Under IR 4402535, Not Robust

05/18/2021

AR 4424747

NRC ID: Action Cancellation Documentation

05/20/2021

AR 4424769

NRC ID: IR Processed as NCAP in Error

05/20/2021

AR 4424800

Actions for IR 2733400 Not Created

05/20/2021

Drawings

M05-1012 Sh. 2

P&ID Cycled Condensate (CY) (Turbine Building)

N

M05-1012 Sh. 6

P&ID Cycled Condensate (CY) (Aux. Fuel & Cont. Building)

X

M05-1074 Sh. 1

P&ID High Pressure Core Spray (HP)

AH

Engineering

Evaluations

CPS-1-2020-

262

DHP Breaker Risk Assessment

Miscellaneous

Operations Department Daily Order

05/17/2021

Nuclear Safety Culture Monitoring Panel Report

03/01/2021

Nuclear Safety Culture Survey #4

03/31/2021

2019-10

Unit 1 Standing Order - DHP Breaker Extent of Condition

FC-00-L

Maintenance Rule System Basis Document - Fuel Pool

Cooling Functions

05/19/2021

FX-03

Maintenance Rule System Basis Document - Flex Spent Fuel

Pool Instruments

05/19/2021

PIAP 2019-0330

Performance Improvement Action Plan - Operations

06/15/2020

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Procedures

3309.01

High Pressure Core Spray (HPCS)

18b

23.05

RCIC Steam Supply Turbine Governing Valve and Linkage

Maintenance (1E51F610)

0e

AD-40.01

Roles and Responsibilities

AR 4202541

DBAI SA, EC 622677 Still at "Assigned" Status

2/12/2018

EI-AA-101

Employee Concerns Program

EI-AA-101-1001

Employee Concerns Program Process

PI-AA-1012

Safety Culture Monitoring

PI-AA-120

Issue Identification and Screening Process

PI-AA-125

Corrective Action Program (CAP) Procedure

PI-AA-125-1001

Root Cause Analysis Manual

PI-AA-125-1003

Corrective Action Program Evaluation Manual

PI-AA-126-1001

Self-Assessments

Self-Assessments AR 1474231

Maintenance ATV-Systematic Approach to Training - 2019

01/01/2020

AR 4139365

2018 Mid Cycle Org Effectiveness Survey Assessment

10/31/2018

AR 4199090

2019 ALARA (Site Review)

2/31/2019

AR 4250915

NOSA-CPS-19-05 Clinton Engineering Design Audit

05/22/2019

AR 4252830-02

SA Report - Exelon 10 CFR 50.59 Review Process

09/30/2019

AR 4296535

20 Clinton Clearance and Tagging Self-Assessment

11/22/2020

AR 4324143

NOSA-CPS-20-03 Clinton Station Emergency Preparedness

Audit

03/05/2020

AR 4338593-04

SA(EP) NRC Emergency Preparedness Program Inspection

08/21/2020

AR 4376069

Preparation for NRC Problem Identification and Resolution

(PI&R) Inspection

03/11/2021

AR 4409641

20 Clinton Safety Culture Assessment

03/19/2021

NOSA-COMP-19-

2019 Operations Comparative Audit Report

11/07/2019

NOSA-CPS-19-

Corrective Action Program Audit Report

03/01/2019

NOSA-CPS-19-

Radiation Protection Audit Report

07/24/2019

NOSA-CPS-20-

Maintenance Functional Area Audit Report

03/11/2020

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

NOSA-CPS-20-

Security Programs Audit Report

2/26/2020

NOSA-CPS-20-

Fitness-for-Duty and Access Authorization Program Audit

Report

08/28/2020