IR 05000461/2020004
| ML21040A365 | |
| Person / Time | |
|---|---|
| Site: | Clinton |
| Issue date: | 02/09/2021 |
| From: | Kenneth Riemer NRC/RGN-III/DRP/B1 |
| To: | Rhoades D Exelon Generation Co, Exelon Nuclear Generation Corp |
| References | |
| IR 2020001 | |
| Download: ML21040A365 (21) | |
Text
February 9, 2021
SUBJECT:
CLINTON POWER STATION - INTEGRATED INSPECTION REPORT 05000461/2020004; 07201046/2020001
Dear Mr. Rhoades:
On December 31, 2020, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Clinton Power Station. On January 14, 2021, the NRC inspectors discussed the results of this inspection with Mr. T. Chalmers, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.
One finding of very low safety significance (Green) is documented in this report. This finding did not involve a violation of NRC requirements.
If you disagree with a cross-cutting aspect assignment or a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; and the NRC Resident Inspector at Clinton Power Station. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Kenneth R. Riemer, Chief Branch 1 Division of Reactor Projects
Docket Nos. 05000461, 07201046
License No. NPF-62
Enclosure:
As stated
Inspection Report
Docket Number:
05000461; 07201046
License Number:
Report Number:
05000461/2020004; 07201046/2020001
Enterprise Identifier: I-2020-004-0059
Licensee:
Exelon Generation Company, LLC
Facility:
Clinton Power Station
Location:
Clinton, IL
Inspection Dates:
October 1, 2020 to December 31, 2020
Inspectors:
J. Beavers, Senior Resident Inspector
J. Dalzell, Reactor Inspector
N. Fields, Reactor Operations Engineer
M. Garza, Emergency Preparedness Inspector
G. Hansen, Sr. Emergency Preparedness Inspector
C. Mathews, Illinois Emergency Management Agency
D. Sargis, Resident Inspector
Approved By:
Kenneth R. Riemer, Chief
Branch 1
Division of Reactor Projects
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Clinton Power Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
List of Findings and Violations
Failure to Determine Extent of Cause Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green FIN 05000461/2020004-01 Open/Closed
[H.12] - Avoid Complacency 71152 The inspectors identified a Green finding when the licensee failed to determine the extent of cause for a root cause in accordance with PI-AA-125-1001, "Root Cause Analysis Manual," Revision 6. Specifically, the licensee failed to identify that lack of technical rigor in the station's FLEX modification caused the FLEX output breaker settings to have been left at factory settings without an analysis.
Additional Tracking Items
None.
PLANT STATUS
Unit 1 operated at or near rated thermal power for the entire inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
Starting on March 20, 2020, in response to the National Emergency declared by the President of the United States on the public health risks of the Coronavirus Disease 2019 (COVID-19), resident inspectors were directed to begin telework and to remotely access licensee information using available technology. During this time, the resident inspectors performed periodic site visits each week; conducted plant status activities as described in IMC 2515, Appendix D, Plant Status; observed risk-significant activities; and completed on-site portions of IPs. In addition, resident and regional baseline inspections were evaluated to determine if all or portions of the objectives and requirements stated in the IP could be performed remotely. If the inspections could be performed remotely, they were conducted per the applicable IP. In some cases, portions of an IP were completed remotely and on-site. The inspections documented below met the objectives and requirements for completion of the IP.
REACTOR SAFETY
71111.01 - Adverse Weather Protection
Seasonal Extreme Weather Sample (IP Section 03.01) (1 Sample)
- (1) The inspectors evaluated readiness for seasonal extreme weather conditions prior to the onset of seasonal cold temperatures for the following systems:
lake/river screen house, fire pump house, and FLEX equipment storage buildings
71111.04 - Equipment Alignment
Partial Walkdown Sample (IP Section 03.01) (6 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
(1)reactor core isolation cooling system on October 8, 2020
- (2) Division 3 emergency diesel generator on November 23, 2020 (3)
'B' control room ventilation train on November 23, 2020 (4)
'C' residual heat removal train on November 24, 2020 (5)
'A' feed water train on November 24, 2020 (6)safety direct current power system on December 2, 2020
71111.05 - Fire Protection
Fire Area Walkdown and Inspection Sample (IP Section 03.01) (6 Samples)
The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:
- (1) Fire Zone A-1b, auxiliary building general access area, elevation 737' on October 6, 2020
- (2) Fire Zone A-1a, auxiliary building general access area, elevation 707' on October 6, 2020
- (3) Fire Zone D-12, diesel generator building Division 1 diesel generator and day tank room, elevation 712' on November 20, 2020
- (4) Fire Zone D-5(a,b), diesel generator building Division 1 diesel fuel tank room, elevation 737' on November 20, 2020
- (5) Fire Zone M-1, screen house Division 1 shutdown service water pump room and Fire Zone M-2(a,b), elevation 699'; Divisions 2 & 3 shutdown service water pump room, elevation 699' on November 20, 2020
- (6) Fire Zone M-3, screen house 'B' fire pump room and Fire Zone M-4, elevation 699';
screen house 'A' fire pump room, elevation 699' on November 20, 2020
Fire Brigade Drill Performance Sample (IP Section 03.02) (1 Sample)
- (1) The inspectors evaluated the onsite fire brigade training and performance during an unannounced fire drill on November 20, 2020.
71111.07A - Heat Sink Performance
Annual Review (IP Section 03.01) (1 Sample)
The inspectors evaluated readiness and performance of:
- (1) Division 4 inverter room cooler 1VX014AA
71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance
Requalification Examination Results (IP Section 03.03) (1 Sample)
- (1) The inspectors reviewed and evaluated the licensed operator examination failure rates for the requalification annual operating exam administered between October 22 and November 20, 2020.
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)
- (1) The inspectors observed and evaluated licensed operator performance in the control room during power restoration from 90 percent to full power, completion of 24-hour Division 1 emergency diesel generator run, and subsequent fast start of Division 1 emergency diesel generator on November 20, 2020.
Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)
- (1) The inspectors observed and evaluated annual dynamic simulator testing on November 18, 2020.
71111.12 - Maintenance Effectiveness
Maintenance Effectiveness (IP Section 03.01) (2 Samples)
The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components remain capable of performing their intended function:
(1)condensate polishing system (2)nuclear system protection system self-testing
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Risk Assessment and Management Sample (IP Section 03.01) (1 Sample)
The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:
(1)planned Yellow risk while switching Division 2 battery to swing battery charger, Work Order 4801239
71111.15 - Operability Determinations and Functionality Assessments
Operability Determination or Functionality Assessment (IP Section 03.01) (3 Samples)
The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:
- (1) Action Request 4373461, "RCIC [reactor core isolation cooling] Pump Oil Cooler Issue"
- (2) Action Request 4376204, "ERAT [emergency reserve auxiliary transformer] Static Var Compensator Thyristor Monitor"
- (3) Action Request 4375036, "Received Unexpected Annunciator 5006-2L, LPRM [local power range monitor] Upscale Alarm"
71111.18 - Plant Modifications
Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1 Sample)
The inspectors evaluated the following temporary or permanent modifications:
(1)revision to secondary containment tornado design criteria
71111.19 - Post-Maintenance Testing
Post-Maintenance Test Sample (IP Section 03.01) (6 Samples)
The inspectors evaluated the following post-maintenance test activities to verify system operability and functionality:
- (1) Work Order 1849500, "Stroke of 1SX041A and 1SX041B after Replacement of Instrument Air Regulator"
- (2) Work Order 4776173, "High Pressure Core Spray Pump Run after System Outage Window"
- (3) Work Order 5058517, "Reactor Core Isolation Cooling Comprehensive Test after System Outage Window"
- (4) Work Order 5088240, "1VF07Y Failed to Open During VG [standby gas treatment]
'A' Shutdown and VF [fuel building ventilation] Startup"
- (5) Work Order 5099146, "Signs of Component Failure 0AP25E-4B (0VC24YB Damper Bucket) after Rebuild"
- (6) Work Order 5099742, "'B' Reactor Recirculating Pump Flow Control Valve"
71111.22 - Surveillance Testing
The inspectors evaluated the following surveillance tests:
Surveillance Tests (other) (IP Section 03.01)
- (1) Work Order 4918018, "Reactor Core Isolation Cooling Remote Shutdown Operability Checks"
- (2) Work Order 4820186, "9080.13 Emergency Diesel Generator 1A 24-Hour Run and Hot Restart"
- (3) Work Order 5093459, "9071.01 Fire Pump 'B' Operability Run"
- (4) Work Order 5048393, "9030.01C06 1B21-N692ABEF Reactor Water Low Level 2 Channel Functional"
71114.02 - Alert and Notification System Testing
Inspection Review (IP Section 02.01-02.04) (1 Sample)
- (1) The inspectors evaluated the following maintenance and testing of the alert and notification system:
- annual siren inspection and maintenance records for the period from September 2018 to September 2020
- monthly alert notification system (siren) tests for the period from September 2018 to September 2020
71114.03 - Emergency Response Organization Staffing and Augmentation System
Inspection Review (IP Section 02.01-02.02) (1 Sample)
- (1) The inspectors evaluated the readiness of the emergency preparedness organization.
71114.04 - Emergency Action Level and Emergency Plan Changes
Inspection Review (IP Section 02.01-02.03) (1 Sample)
- (1) The inspectors completed an evaluation of submitted emergency action level and emergency plan changes on December 2, 2020. This evaluation does not constitute NRC approval.
71114.05 - Maintenance of Emergency Preparedness
Inspection Review (IP Section 02.01 - 02.11) (1 Sample)
- (1) The inspectors evaluated the maintenance of the emergency preparedness program.
OTHER ACTIVITIES - BASELINE
===71151 - Performance Indicator Verification
The inspectors verified licensee performance indicators submittals listed below:
EP01: Drill/Exercise Performance (IP Section 02.12)===
(1)01/01/2019 - 06/30/2020
EP02: ERO Drill Participation (IP Section 02.13) (1 Sample)
- (1) 01/01/2019 - 06/30/2020
EP03: Alert & Notification System Reliability (IP Section 02.14) (1 Sample)
- (1) 01/01/2019 - 06/30/2020
71152 - Problem Identification and Resolution
Annual Follow-up of Selected Issues (IP Section 02.03) (2 Samples)
The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:
- (1) FLEX diesel generator breaker set to factory settings (2)unplanned reactivity events during
OTHER ACTIVITIES
- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL
60855.1 - Operation of an Independent Spent Fuel Storage Installation at Operating Plants Operation of an Independent Spent Fuel Storage Installation at Operating Plants
- (1) The inspectors evaluated the licensees activities related to the long-term operation and monitoring of its independent spent fuel storage installation (ISFSI). The inspectors reviewed relevant documentation and interviewed personnel remotely during the week of November 16, 2020. The inspector performed an onsite walkdown of the ISFSI pad and haul path and evaluated the material condition of the ISFSI pad and HI-STORM FW casks on November 16, 2020. The inspector utilized licensee personnel and radiological instrumentation to verify that radiological conditions on the ISFSI pad were as expected during the walkdown.
The inspectors evaluated the following change reviews:
- changes to the licensee's 10 CFR 72.212 report performed since October 1, 2018
- 10 CFR 72.48 screenings and a 10 CFR 72.48 evaluation performed since October 1, 2018
- procedural changes primarily stemming from lessons learned or operating experience since the licensee's previous loading campaign
INSPECTION RESULTS
Failure to Determine Extent of Cause Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems
Green FIN 05000461/2020004-01 Open/Closed
[H.12] - Avoid Complacency 71152 The inspectors identified a Green finding when the licensee failed to determine the extent of cause for a root cause in accordance with PI-AA-125-1001, "Root Cause Analysis Manual,"
Revision 6. Specifically, the licensee failed to identify that lack of technical rigor in the station's FLEX modification caused the FLEX output breaker settings to have been left at factory settings without an analysis.
Description:
On June 26, 2020, the licensee wrote Action Request 4352937 documenting that the FLEX diesel generator output breakers did not have an engineering analysis to determine the correct breaker settings. Both FLEX diesel generator output breakers were still set to the factory default settings. Upon discovery of the condition, it was uncertain if the FLEX diesel generators would have been able to supply power without tripping the output breaker. The licensee evaluated the condition and determined that the breaker would not trip if it were supplying power and that there was less margin in the calculation than would normally be acceptable. The licensee adjusted the breaker settings to provide a more acceptable margin.
The licensee performed a corrective action program evaluation for the condition and identified that the breaker settings were not discussed in Engineering Change 392335, which installed the breakers. The licensee determined that the cause was less than adequate technical rigor by the engineer responsible for the FLEX modification. The inspectors noted that this cause was nearly identical to the cause identified in Root Cause Report 4297570 for the FLEX diesel generator 1FX01KA being wired with its phase rotation out of phase from the plant equipment phase rotation. The phase rotation issue was previously identified as a Green finding identified in NRC integrated inspection report 05000461/2020001 as FIN 05000461/2020001-01 "FLEX Diesel Generator Phase Rotation Incorrect."
The inspectors reviewed Root Cause Report 4297570 to determine the similarities between the FLEX diesel generator phase rotation issue and the output breaker settings issue. The root cause identified was that engineers did not apply technical human performance fundamentals during selection of post-modification testing for the FLEX modification. The licensee conducted an extent-of-cause review for the root cause in accordance with PI-AA-125-1001, "Root Cause Analysis Manual," Revision 6. The extent-of-cause review evaluated all modifications that were completed by the responsible engineers to verify that post-modification testing was correct. The extent-of-cause did not review the modifications to verify overall adequacy or that the appropriate engineering rigor was applied to areas outside of post-modification testing.
Exelon procedure PI-AA-125-1006, "Investigation Techniques Manual," Revision 5, includes considerations for performing an extent-of-cause review. The manual stresses the importance of identifying how a cause could affect programs or processes other than the one that was already identified. When the licensee focused their extent-of-cause review on the adequacy of post-modification testing, they did not consider how the cause could affect other processes or programs that could have been affected by lack of technical rigor in implementing the FLEX modification. Specifically, the review did not identify that Engineering Change 392335 did not provide any analysis of the FLEX breakers; therefore, the breakers did not have any discussion for post-modification testing.
Corrective Actions: The licensee determined correct breaker settings and performed the change to support breaker functionality.
Corrective Action References: Action Request 4352937, "FLEX Diesel Generator Breaker Settings"
Performance Assessment:
Performance Deficiency: The licensee failed to determine the extent of cause for a root cause as required by PI-AA-125-1001. This led to the licensee failing to identify that the FLEX diesel generator output breaker settings were not evaluated and were set to factory default settings instead of site-specific settings.
Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Design Control attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, there was reasonable doubt as to the functionality of the FLEX generator output breakers until a detailed analysis was performed, and following the analysis, the licensee determined that the settings should be revised. This was similar to example 3.a in Inspection Manual Chapter 0612, Appendix E, "Examples of Minor Issues."
Significance: The inspectors assessed the significance of the finding using Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors used Exhibit 2, "Mitigating Systems Screening Questions," Section E "Flexible Coping Strategies (FLEX)," and answered "No" to all questions. Therefore, the finding screens to Green or very low safety significance.
Cross-Cutting Aspect: H.12 - Avoid Complacency: Individuals recognize and plan for the possibility of mistakes, latent issues, and inherent risk, even while expecting successful outcomes. Individuals implement appropriate error reduction tools. Specifically, when the licensee attempted to identify the extent of cause for the FLEX diesel generator phase rotation issue; they only focused on post-modification testing and did not attempt to identify other areas where lack of technical rigor could have impacted the FLEX implementation.
Enforcement:
Inspectors did not identify a violation of regulatory requirements associated with this finding.
Observation: Unplanned Reactivity Events in 2020 71152 The inspectors observations and assessments of trends related to several unplanned power changes over 2020 indicated an inconsistent range of response in assessment as well as communication with the support organizations and management. The inspectors determined that the lack of an off normal procedure to address unplanned power changes impacted the consistent application of process in both response and communication. All minor issues with each event were individually addressed in the quarter in which they occurred during the quarterly exits. The station did take note of the inspectors observations regarding the response to these events and is developing an off normal response procedure for unplanned power changes. The procedure is slated for completion by the first half of
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
- On January 14, 2021, the inspectors presented the integrated inspection results to Mr. T. Chalmers, Site Vice President, and other members of the licensee staff.
- On October 15, 2020, the inspectors presented the emergency preparedness baseline inspection results to Mr. J. Kowalski, Plant Manager, and other members of the licensee staff.
- On November 20, 2020, the inspectors presented the independent spent fuel storage installation (ISFSI) program review inspection results to Mr. T. Chalmers, Site Vice President, and other members of the licensee staff.
- On December 2, 2020, the inspectors presented the IP 71114.04 exit meeting inspection results to Mr. D. Moore, Senior Manager - Emergency Preparedness, and other members of the licensee staff.
- On December 14, 2020, the inspectors presented the annual licensed operator requalification examination inspection results to Mr. R. Tyler, Licensed Operator Lead Instructor, and other members of the licensee staff.
DOCUMENTS REVIEWED
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
60855.1
Corrective Action
Documents
Selected Corrective Action Documents Created Since
October 2018
60-Day Reporting Period for ISFSI ARERR Not Met
04/04/2019
Unexpected Water Flowing Out of the MPC Drain Port
07/07/2020
Forced Helium Drying Skid Issue: Braidwood
09/18/2020
Corrective Action
Documents
Resulting from
Inspection
Errors in Survey Calculations
11/18/2020
Spalling on South West Edge of ISFSI Pad
11/19/2020
Engineering
Changes
ECO 5018-65
Holtec Engineering Change Order
ISFSI 72.212-CR-
2018-001, ISFSI
2.212-CR-2018-
2, ISFSI 72.212-
CR-2018-003, ISFSI
2.212-CR-2018-
004, ISFSI 72.212-
CR-2019-001
2.212 Evaluation Report Change Requests
Miscellaneous
Clinton Power Station Unit 1 10 CFR 72.212 Evaluation
Report for the HI-STORM FW MPC Storage System
Docket 72-1046
2018 Annual Radiological Environmental Operating
Report Clinton Power Station - Docket Number 50-461
04/25/2019
2019 Annual Radiological Environmental Operating
Report Clinton Power Station - Docket Number 50-461
04/28/2020
2.48
Screening/Evaluation
209
Holtec 10 CFR 72.48 Screening/Evaluation for ECO
5018-65
0, 1
2.48-CL-2018-S-
2, 72.48-CL-2018-
S-023, 72.48-CL-
2018-S-024, 72.48-
CFR 72.48 Screenings and Evaluations
October
2018 to
October
20
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
CL-2018-E-024,
2.48-CL-2018-S-
25, 72.48-CL-2018-
S-026, 72.48-CL-
2019-S-001, 72.48-
CL-2020-S-001
Addendum 3
Emergency Action Levels for Clinton Station
Quality Assurance Topical Report
Clinton Power Station, October 1, 2016 to September 30,
2017, Independent Spent Fuel Storage Installation Annual
Radioactive Effluent Release Report
04/24/2019
Clinton Power Station, October 1, 2017 to
September 30, 2018, Independent Spent Fuel Storage
Installation Annual Radioactive Effluent Release Report
04/25/2019
Clinton Power Station, October 01, 2018 to September
30, 2019, Independent Spent Fuel Storage Installation
Annual Radioactive Effluent Release Report
11/13/2020
Clinton Power Station, October 01, 2019 to September
30, 2020, Independent Spent Fuel Storage Installation
Annual Radioactive Effluent Release Report
11/13/2020
Procedures
CPS 1019.05
Transient Equipment/Materials
CPS 1860.01C001
Operations Department Cold Weather Preparations
Checklist
9b
CPS 1893.04M913
Independent Spent Fuel Storage Facility Installation
(ISFSFI) Prefire Plan
0a
CPS 9000.01D001
Control Room Surveillance Log - Mode 1, 2, 3 Data Sheet
58d
CPS 9000.01D002
Control Room Surveillance Log - Mode 4, 5 Data Sheet
Environmental Dosimetry - Performance Specifications,
Testing, and Data Analysis
Structures Monitoring
HPP-2226-200
MPC Loading at Clinton
HPP-2226-400
MPC Transfer at Clinton
HPP-2226-500
HI-STORM Movements
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
HPP-2226-600
MPC Unloading at Clinton
HPP-2226-700
Responding to Abnormal Conditions
OP-AA-108-111-
1001
Severe Weather and Natural Disaster Guidelines
Conduct of Outage Services Manual T&RM
Spent Fuel Loading Campaign Management
Dry Cask Storage/ISFSI Inspection Surveillance Program
OU-CL-800-81
DCS Campaign Preparations and Restoration
OU-CL-800-83
Spent Fuel Cask Contingency Actions
Holtec HI-TRAC Radiation Survey
Holtec HI-STORM Radiation Survey
Holtec Independent Spent Fuel Storage Installation
(ISFSI) Radiation Survey
Controls for Independent Spent Fuel Storage (ISFSI)
Associated Activities
Radiation
Surveys
2019-046314
Outside Areas - ISFSI Pad Grid Survey
(per RP-CL-300-1004 - Sections 5.1-5.3)
06/15/2019
2019-046316
Outside Areas - ISFSI Pad Protected Area Fence Survey
(per RP-CL-300-1004 - Section 5.4)
06/15/2019
20-072193
Outside Areas - ISFSI Pad
05/04/2020
20-080757
Outside Areas - ISFSI Pad Grid Survey
(per RP-CL-300-1004 - Sections 5.1-5.3)
09/26/2020
20-080759
Outside Areas - ISFSI Pad Protected Area Fence Survey
(per RP-CL-300-1004 - Section 5.4)
09/26/2020
Self-
Assessments
AR 429608-02
Clinton Spent Fuel Loading Readiness Assessment
07/29/2020
NOSA-CPS-18-10
Independent Spent Fuel Storage Installation Audit Report:
Clinton Power Station
11/14/2018
NOSA-CPS-20-10
Independent Spent Fuel Storage Installation Audit Report
10/02/2020
Work Orders
ISFSI - DCS Eng Perform Annual Insp of ISFSI per
OU-CL-630-100
08/14/2019
OP 9000.01 Control Room Surv Log for Mode 1/2/3,
D001-Weekly
11/17/2019
OP 9000.01 Control Room Surv Log for Mode 1/2/3,
03/08/2020
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
D001-Weekly
ISFSI - DCS Eng Perform Annual Insp of ISFSI per
OU-CL-630-100
08/12/2020
Procedures
Seasonal Readiness
Drawings
M05-1004, Sheet 1
AH
Procedures
CPS 3310.01V001
Reactor Core Isolation Cooling Valve Lineup
CPS 3312.01V001
Residual Heat Removal Valve Lineup
17c
CPS 3402.01E001
Control Room HVAC Electrical Lineup
10e
CPS 3506.01C003
Diesel Generator 1C Pre-Start Checklist
6e
Fire Plans
CPS 1893.04M100
707 Auxiliary Building General Access Area Prefire Plan
5a
CPS 1893.04M110
737 Auxiliary Building General Access Area Prefire Plan
6b
Procedures
CPS 1893.04M511
737 Diesel Generator Building Div 1 Diesel Generator &
Day Tank Room
6c
CPS 1893.04M800
699 Screen House Div 1 SX Pump Room Prefire Plan
5a
CPS 1893.04M801
699 Screen House Div 2&3 SX Pump Rooms and Tunnel
Prefire Plan
6a
CPS 1893.04M802
699 Screen House 'B' Fire Pump Room Prefire Plan
6a
CPS 1893.04M803
699 Screen House 'A' Fire Pump Room Prefire Plan
6a
Work Orders
Inspect, Boroscope, Clean, Eddy Current, and Hydrolase
as Required
05/12/2020
Procedures
TQ-AA-150-F25
Clinton 2020 LORT Annual Exam Status Report
2/07/2020
71111.11Q Miscellaneous
ESG-LOR-10
Clinton Power Station Licensed Operator Training
Simulator Exercise Guide
Work Orders
OP Cross-Tie Div II DC MCC 1B / Swing Charger
1DC11E
10/26/2020
Work Orders
OP 9054.01C002 RCIC 1E51-C001 High Pressure
Operability Check
09/24/2020
1VF07Y Failed to Open During VG 'A' Shutdown and VF
Startup
10/27/2020
0AP25E-4B (0VC24YB Damper Bucket) Rebuild
Leakcheck RR Subloop B1
Corrective Action
Documents
ATM B21N692B and F Gross Fail High Didn't Come in As
Expected
09/25/2020
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Work Orders
OP 9054.05 RCIC Remote Shutdown Panel Operability
Checks
09/24/2020
9030.01C06 Channel Functional RCIC Reactor Low Level
B21-N692ABEF
09/25/2020
9071.01B21 Fire Pump Operability Run
11/23/2020
Corrective Action
Documents
EP-Siren Failures (CL06 & CL21)
06/19/2019
EP ID: Trend IR; Multiple CPS Siren Failures
07/08/2019
EP - Dewitt County Siren Controller Inoperable
04/17/2020
Miscellaneous
Exelon Nuclear Manager, Midwest Emergency
Preparedness Letter to Program Enhancement Manager,
Illinois Emergency Management Agency; Submission of
Clinton Power Station Public Alert and Notification System
(ANS) Design Report, Revision 3
10/01/2018
Clinton Station Monthly Siren Availability Reports
09/01/2018 -
09/30/2020
Clinton Primary Notification System (PNS) Maintenance
Reports
09/01/2018 -
09/30/2018
Semi-Annual Clinton Power Siren Reports
09/01/2018 -
09/30/2020
2019/2020 Emergency Planning for the Clinton Area
(Community Information Booklet)
07/19/2019
20/2021 Emergency Planning for the Clinton Area
(Community Information Booklet)
06/17/2020
- U.S. Department of Homeland Security, FEMA Letter,
Subj: Backup Alert and Notification System
2/10/2012
KLD-TR-987
Clinton Power Station Alert and Notification System (ANS)
Design Report
09/19/2018
Procedures
EP-AA-120-F-02
EP Staff Initial Developmental Checklist
H
TSC Activation and Operation
OSC Activation and Operation
EOF Activation and Operation
Corrective Action
Documents
EP ID: 1 Hour Responder Failed to Call During
Augmentation Drill
09/14/2018
EP ID: 2nd Quarter ERO Augmentation Drill
05/17/2019
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Miscellaneous
Quarterly Unannounced Off-Hours Call-In Augmentation
Drill Results
09/01/2018 -
09/30/2020
Emergency Response Organization Duty Roster
09/22/2020
Procedures
Addendum 1
On-Shift Staffing Technical Basis
Emergency Response Organization (ERO)/Emergency
Response Facility (ERF) Activation and Operation
EP-AA-112-100-F-06 ERO Notification or Augmentation
X
ERO Training and Qualification
Corrective Action
Documents
Perform Impact Review of EAL Revisions from
EOP/SAMG, Rev. 4
03/10/2020
NOS ID: Revise Standardized Emergency Plan
03/26/2020
EPlan: CDAM 50.54(q) Potential Deficiencies
04/09/2020
Miscellaneous
Eval No. 19-29
Exelon Nuclear Standardized Radiological Emergency
Plan
09/04/2020
Eval No. 19-65
Exelon Nuclear Standardized Radiological Emergency
Plan
09/06/2019
Eval No. 19-79
Various Station Emergency Plan Annexes
11/08/2019
Eval No. 19-80
On-Shift Staffing Assessments
11/08/2019
Corrective Action
Documents
NOS ID: Increase communication with Warner Hospital
04/15/2020
Communicate with Maroa FD About Their EP Role
04/15/2020
NOS ID: Satellite Testing not Conducted by Required
Disciplines
04/15/2020
Exercise/Drill Evaluated Reports and Communication Test
Forms Contain Documentation Errors
04/15/2020
Annual Testing not Performed on 47 of 259 Public
Address (PA) Speakers in 2019
04/16/2020
Miscellaneous
Full Scale PI Drill Series Report
2/19/2018
Clinton 2020 1st Half Health Physics Drill Report
07/22/2020
Clinton Medical/Health Physics Drill Evaluation Report
11/15/2019
Clinton 2019 NRC Graded Exercise Evaluation Report
04/18/2019
03/09/2020
2019 NRC Pre-Exercise WANO Emergency Management
03/11/2019
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Performance Evaluation
Clinton 2019 1st Half Health Physics Drill Report
05/31/2019
EP-AA-124-F-01
Quarterly Emergency Response Data System (ERDS)
Test Records
09/01/2018 -
09/30/2020
EP-MW-124-1001-F-
Control Room/Simulator Inventory Records
09/01/2018 -
09/30/2020
EP-MW-124-1001-F-
CR/Simulator/TSC/OSC Equipment Test-TSC Software
and Reference Document Inventory Records
09/01/2018 -
09/30/2020
EP-MW-124-1001-F-
Technical Support Center Inventory Records
09/01/2018 -
09/30/2020
EP-MW-124-1001-F-
Operations Support Center Inventory Records
09/01/2018 -
09/30/2020
EP-MW-124-1001-F-
Field Team Inventory Records
09/01/2018 -
09/30/2020
EP-MW-124-1001-F-
Assembly Area Inventory Records
09/01/2018 -
09/30/2020
EP-MW-124-1001-F-
Medical Response Kit Inventory Records
09/01/2018 -
09/30/2020
EP-MW-124-1001-F-
Monthly NARS Communications Test Records
09/01/2018 -
09/30/2020
EP-MW-124-1001-F-
Monthly ENS Communications Test Records
09/01/2018 -
09/30/2019
EP-MW-124-1001-F-
Quarterly Directors Hotline Test Records
09/01/2018 -
09/30/2020
EP-MW-24-1001-F-
Quarterly Operations Status Line Test Records
09/01/2018 -
09/30/2020
EP-MW-124-1001-F-
Quarterly Damage Control Line Test Records
09/01/2018 -
09/30/2020
EP-MW-124-1001-F-
Quarterly Technical Support Line Test Records
09/01/2018 -
09/30/2020
KLD-TR-1002
Clinton Power Station 2018 Population Update Analysis
09/08/2018
KLD-TR-1181
Clinton Power Station 2020 Population Update Analysis
09/05/2020
Procedures
Exelon Nuclear Standardized Radiological Emergency
Plan
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Exelon Nuclear Radiological Emergency Plan Annex for
Clinton Station
Addendum 2
Evacuation Time Estimates for Clinton Power Station
Plume Exposure Pathway Emergency Planning Zone
EP-AA-122; Drills and Exercise Program
Inventories and Surveillances
Self-
Assessments
NOSA-CPS-19-03
Emergency Preparedness Audit Report
03/15/2019
NOSA-CPS-20-03
Emergency Preparedness Audit Report
04/22/2020
71151
Miscellaneous
NRC Performance Indicator Data; Emergency
PreparednessDrill/Exercise Performance
01/01/2019 -
06/30/2020
NRC Performance Indicator Data; Emergency
PreparednessERO Readiness
01/01/2018 -
06/30/2020
NRC Performance Indicator Data; Emergency
PreparednessAlert and Notification System Reliability
01/01/2018 -
06/30/2020