IR 05000277/2012005

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IR 05-277-12-005 and 05-278-12-005, on 10/01/2012 - 12/31/2012, Peach Bottom Atomic Power Station - NRC Integrated Inspection Report
ML13029A013
Person / Time
Site: Peach Bottom  Constellation icon.png
Issue date: 01/29/2013
From: Gray M K
Reactor Projects Region 1 Branch 4
To: Pacilio M J
Exelon Nuclear, Exelon Generation Co
GRAY, MEL
References
IR-12-005
Download: ML13029A013 (48)


Text

January 29, 2013

Mr. Michael Senior Vice President, Exelon Generation Company, LLC President and Chief Nuclear Officer, Exelon Nuclear 4300 Winfield Road Warrenville, IL 60555

SUBJECT: PEACH BOTTOM ATOMIC POWER STATION - NRC INTEGRATED INSPECTION REPORT 05000277/2012005 AND 05000278/2012005

Dear Mr. Pacilio:

On December 31, 2012, the U. S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Peach Bottom Atomic Power Station (PBAPS), Units 2 and 3. The enclosed integrated inspection report documents the inspection results, which were discussed on January 18, 2013, with Mr. Michael Massaro, Site Vice President, and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

Based on the results of this inspection, no findings were identified. However, three licensee-identified violations, which were determined to be of very low safety significance, are listed in this report. However, because of the very low safety significance, and because they are entered into your corrective action program (CAP), the NRC is treating these findings as non-cited violations (NCVs), consistent with Section 2.3.2 of the NRC Enforcement Policy. If you contest any NCVs in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the PBAPS.

In accordance with Title 10 of the Code of Federal Regulations (10 CFR), Section 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,/RA/

Mel Gray, Chief Reactor Projects Branch 4 Division of Reactor Projects Docket Nos.: 50-277, 50-278 License Nos.: DPR-44, DPR-56

Enclosure:

Inspection Report 05000277/2012005 and 05000278/2012005

w/Attachment:

Supplementary Information

cc w/encl: Distribution via ListServ

SUMMARY OF FINDINGS

........................................................................................................... 3

REPORT DETAILS

REACTOR SAFETY

.................................................................................................................. 4 1R01 Adverse Weather Protection .................................................................................... 4 1R04 Equipment Alignment ............................................................................................... 5 1R05 Fire Protection .......................................................................................................... 6 1R06 Flood Protection Measures ...................................................................................... 7 1R11 Licensed Operator Requalification Program ............................................................ 7 1R12 Maintenance Effectiveness ...................................................................................... 8 1R13 Maintenance Risk Assessments and Emergent Work Control ................................. 8 1R15 Operability Determinations and Functionality Assessments .................................... 9 1R19 Post-Maintenance Testing ..................................................................................... 10 1R20 Refueling Outage .................................................................................................... 10 1EP6 EP Drill Evaluation

RADIATION SAFETY

.............................................................................................................. 12

2RS5 Radiation Monitoring Instrumentation

.................................................................... 12

2RS6 Radioactive Gaseous and Liquid Effluent Treatment

OTHER ACTIVITIES

............................................................................................................... 16

4OA1 Performance Indicator Verification

......................................................................... 16

4OA2 Identification and Resolution of Problems ............................................................... 17 4OA3 Follow-up of Events and Notices of Enforcement Discretion

................................. 19

4OA5 Other Activities ........................................................................................................ 20 4OA6 Meetings, Including Exit .......................................................................................... 26 4OA7 Licensee-Identified Violations ................................................................................. 26

ATTACHMENT:

SUPPLEMENTARY INFORMATION

KEY POINTS OF CONTACT

.................................................................................................... A-1

LIST OF ITEMS

OPENED, CLOSED, DISCUSSED ................................................................ A-1

LIST OF DOCUMENTS REVIEWED

........................................................................................ A-2

LIST OF ACRONYMS

............................................................................................................. A-16

Enclosure

SUMMAR Y
OF [[]]
FINDIN [[]]

GS IR 05000277/2012005, 05000278/2012005; 10/01/2012 - 12/31/2012; Peach Bottom Atomic

Power Station (PBAPS), Units 2 and 3; Integrated Inspection.

The report covered a three-month period of inspection by resident inspectors and announced

inspections performed by regional inspectors. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP). The cross-cutting aspects for the findings were

determined using

IMC 0310, "Components Within Cross-Cutting Areas." Findings for which the
SDP does not apply may be Green, or be assigned a severity level after

NRC management

review. The

NRC 's program for overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity None.

Other Findings Three violations of very low safety significance, which were identified by Exelon personnel, have been reviewed by the inspectors. Corrective actions taken or planned by Exelon have been entered into the corrective action program (CAP). These violations and the corrective action tracking numbers are listed in Section 4OA7 of this report.

Enclosure

REPORT [[]]

DETAILS Summary of Plant Status

Unit 2 began the inspection period shutdown for the 19th refueling outage (RFO) (P2R19). On October 17, 2012, the reactor mode switch was placed in start-up and the unit was

synchronized to the grid on October 19. On October 21, the unit was returned to 100 percent

rated thermal power (RTP). Unit 2 remained at RTP until the end of the inspection period, except for brief periods to support planned testing and control rod pattern adjustments.

Unit 3 began the inspection period at 100 percent RTP. On November 10, operators reduced

power to approximately 70 percent to perform main turbine control valve trouble-shooting and repair, and a control rod pattern adjustment. The unit was returned to 100 percent

RTP the next day. The unit remained at

RTP through the end of the inspection period, except for brief periods to support planned testing and control rod pattern adjustments.

1.

REACTO R

SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity 1R01 Adverse Weather Protection (71111.01 - 2 samples)

.1 Super Storm Sandy (1 Grid sample) a. Inspection Scope

The inspectors reviewed plant features and procedures for operation and continued availability

of offsite and backup power systems during Super Storm Sandy on October 30, 2012. The 500

Kilovolt (KV) grid voltage reached a maximum voltage of

550KV due to the reduced grid electrical demand during the storm. The inspectors reviewed the control room operator response to Alarm Response Card (
ARC ), "South
500 KV Sub-Station General Alarm,"

ARC-

006 00C224 J-5, Revision 2, and procedure AO 53.2-0, "Equipment Checks After a

Thunderstorm," Revision 4. The inspectors reviewed communication protocols between the

control room personnel and electrical system operations, as well as measures prescribed and taken to maintain the availability and reliability of alternating current systems during the abnormal high grid voltage.

Additionally, the inspectors reviewed procedures for severe weather preparation, main control

room (MCR) logs, and condition reports (CRs). Documents reviewed for each section of this inspection report are listed in the Attachment. b. Findings

No findings were identified.

.2 Readiness for Seasonal Extreme Weather Conditions (1 Seasonal sample) a. Inspection Scope

The inspectors performed a review of

PBA [[]]

PS's readiness for the onset of seasonal cold

temperatures. The review focused on the auxiliary boiler system heating steam supply,

Enclosure emergency diesel generators (EDGs), emergency cooling tower (ECT), emergency service water (ESW) and high pressure service water (HPSW) pump rooms, outer intake cooling water pump structure building, and the inner intake cooling water screen structure. The inspectors reviewed the Updated Final Safety Analysis Report (UFSAR), Technical Specifications (TSs), control room logs, and the CAP to determine what temperatures or other seasonal weather

could challenge these systems, and to ensure

PBA [[]]

PS personnel had adequately prepared for

these challenges. The inspectors reviewed station procedures, including

PBA [[]]

PS's seasonal weather preparation procedure and applicable operating procedures. The inspectors performed walkdowns of the selected systems to ensure station personnel identified issues that could challenge the operability of the systems during cold weather conditions. The inspectors also

reviewed

CAP items to verify that

PBAPS was identifying adverse weather issues at an

appropriate threshold and entering them into their CAP in accordance with station corrective

action procedures. Documents reviewed for each section of this inspection report are listed in the Attachment.

b. Findings

No findings were identified.

1R04 Equipment Alignment (71111.04 - 5 samples)

.1 Partial System Walkdowns (71111.04Q - 4 samples)

a. Inspection Scope The inspectors performed partial walkdowns of the following four systems: All four

EDG s during Super Storm Sandy on October 30 Unit 3 'B' train of residual heat removal (

RHR) with 'A' train unavailable on November 13 and 14 Unit 3 4Kv electrical buses with offsite power startup source 343 out-of-service (OOS) on November 29 Unit 2 125 volt direct current (DC) electrical buses during yellow risk on November 28

The inspectors selected these systems based on their risk-significance relative to the

reactor safety cornerstones at the time they were inspected. The inspectors reviewed applicable operating procedures, system diagrams, the

UFSAR ,

TSs, work orders (WOs), CRs, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have impacted system performance of their intended safety functions. The inspectors also performed field walkdowns of accessible

portions of the systems to verify system components and support equipment were aligned correctly and were operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no deficiencies. The inspectors also reviewed whether

PBA [[]]

PS staff had properly

identified equipment issues and entered them into the CAP for resolution with the

appropriate significance characterization. b. Findings

No findings were identified.

Enclosure .2 Full System Walkdown (71111.04S - 1 sample) a. Inspection Scope On December 11 and 12, 2012, the inspectors performed a complete system walkdown

of accessible portions of the 'B' train of ESW to verify the existing equipment lineup was

correct while the 'A' train was unavailable for planned maintenance. The inspectors

reviewed operating procedures, surveillance tests (STs), drawings, equipment line-up check-off lists, and the

UFS [[]]

AR to verify the system was aligned to perform its required safety functions. The inspectors also reviewed electrical power availability, component

lubrication and equipment cooling, hangar and support functionality, and operability of

support systems. The inspectors performed field walkdowns of accessible portions of

the systems to verify system components and support equipment were aligned correctly and operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no deficiencies.

Additionally, the inspectors reviewed a sample of related

CR s and work orders (

WOs) to

ensure

PBA [[]]

PS staff appropriately evaluated and resolved any deficiencies.

b. Findings No findings were identified.

1R05 Fire Protection (71111.05Q - 7 samples) .1 Resident Inspector Quarterly Walkdowns

a. Inspection Scope The inspectors conducted tours of the areas listed below to assess the material condition and operational status of fire protection features. The inspectors verified that

PBA [[]]

PS controlled combustible materials and ignition sources were controlled in

accordance with administrative procedures. The inspectors verified that fire protection

and suppression equipment was available for use as specified in the area pre-fire plan,

and passive fire barriers were maintained in good material condition. The inspectors

also verified that station personnel implemented compensatory measures for

OOS , degraded or inoperable fire protection equipment, as applicable, in accordance with procedures. Unit 2 circulating water pump structure on November 7 Unit 3 circulating water pump structure on November 7 Unit 3 'B' and 'D'
RHR pump and heat exchanger (HX) rooms on November 13 Unit 2 refuel floor on December 10 Unit 2 'B' and 'D'
RHR pump and

HX rooms on December 12 Unit 2 reactor building (RB) 135' elevation on December 13 ECT structure on December 18

Enclosure b. Findings No findings were identified.

1R06 Flood Protection Measures (71111.06 - 1 sample)

.1 Internal Flooding Reviews a. Inspection Scope

The inspectors reviewed the

UFS [[]]

AR, the site flooding analysis, and plant procedures to

assess susceptibilities involving internal flooding. The inspectors also reviewed the

CAP to determine if
PBA [[]]

PS personnel identified and corrected flooding problems and whether operator actions for coping with flooding were adequate. The inspectors focused on the safety-related pump structure to verify the adequacy of equipment seals located below

the flood line, floor and water penetration seals, watertight door seals, common drain

lines and sumps, sump pumps, level alarms, control circuits, and temporary or

removable flood barriers. b. Findings No findings were identified.

1R11 Licensed Operator Requalification Program (71111.11 - 2 samples) .1 Quarterly Review of Licensed Operator Requalification Testing and Training

a. Inspection Scope The inspectors observed licensed operator requalification simulator training on November 28, 2012, which included high reactor recirculation pump (RRP) vibration,

loss of an auxiliary electrical bus including the second RRP, manual reactor scram, and

the restart of one RRP. The inspectors evaluated operator performance during the

simulated events and verified completion of risk significant operator actions, including

the use of abnormal and emergency operating procedures. The inspectors assessed the clarity and effectiveness of communications, implementation of actions in response to alarms and degrading plant conditions, and the oversight and direction provided by

the control room supervisor. The inspectors verified the accuracy and timeliness of the

emergency classification made by the shift manager, and the TS action statements

entered by the shift technical advisor. Additionally, the inspectors assessed the ability of the crew and training staff to identify and document crew performance problems. b. Findings No findings were identified.

Enclosure .2 Quarterly Review of Licensed Operator Performance in the Main Control Room a. Inspection Scope The inspectors observed the following activity in the main control room (MCR): Off-site power transformer 343 start-up source restoration The inspectors observed infrequently performed tests or evolution briefings, pre-shift

briefings, and reactivity control briefings to verify that the briefings met the criteria specified in Exelon's procedure

HU -

AA-1211, "Pre-Job Briefings," Revision 7. Additionally, the inspectors observed test performance to verify that procedure use, crew

communications, and coordination of activities between work groups similarly met established expectations and standards. b. Findings No findings were identified.

1R12 Maintenance Effectiveness (71111.12Q - 2 samples) a. Inspection Scope The inspectors reviewed the samples listed below to assess the effectiveness of

maintenance activities on structures, systems, and components (SSCs) performance

and reliability. The inspectors reviewed system health reports,

CAP documents, maintenance
WO s, and maintenance rule (MR) basis documents to ensure that
PBA [[]]
PS was identifying and properly evaluating performance problems within the scope of the
MR. For each sample selected, the inspectors verified that the

SSC was properly

scoped into the

MR in accordance with 10

CFR 50.65 and verified that the (a)(2)

performance criteria established by the

PBAPS staff were reasonable. As applicable, for
SSC s classified as (a)(1), the inspectors assessed the adequacy of goals and corrective actions to return these
SSC s to (a)(2). Additionally, the inspectors ensured that

PBAPS staff was identifying and addressing common cause failures that occurred within and

across MR system boundaries.

Unit 2 average power range monitor (APRM) 2-out-of-4 voter failure on November 1 Diesel driven fire pump 'A' battery charger high amp reading on November 19 and November 21 b. Findings No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - 4 samples) a. Inspection Scope The inspectors reviewed station evaluation and management of plant risk for the

maintenance and emergent work activities listed below to verify that

PBA [[]]

PS performed the appropriate risk assessments prior to removing equipment for work. The inspectors selected these activities based on potential risk significance relative to the reactor safety

Enclosure cornerstones. As applicable for each activity, the inspectors verified that

PBAPS personnel performed risk assessments as required by 10
CFR 50.65(a)(4) and that the assessments were accurate and complete. When
PBA [[]]

PS performed emergent work, the inspectors verified that operations personnel promptly assessed and managed plant

risk. The inspectors reviewed the scope of maintenance work and discussed the results

of the assessment with the station's probabilistic risk analyst to verify plant conditions

were consistent with the risk assessment. The inspectors also reviewed the

TS requirements and inspected portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met. Elevated risk during
ST -O-052-122-2, "E-2
EDG [[]]
RHR Pump Reject Test," Revision 9, on November 5 Elevated risk with 3 'A'
RHR [[]]
OOS on November 13 and 14 Unit 3 'F' reactor recirculation jet pump flow deviations on November 19 Elevated risk during E-1

EDG unavailability for planned maintenance on December 11 and 12

b. Findings No findings were identified. 1R15 Operability Determinations and Functionality Assessments (71111.15 - 5 samples)

a. Inspection Scope

The inspectors reviewed five operability determinations (ODs) for the following degraded or non-conforming conditions: Unit 2 wide-range neutron monitoring (WRNM) during core reload on October 10 Unit 2 and Unit 3 reactor water cleanup (RWCU) motor-operated valve (MOV) primary containment isolation valve operability evaluations on October 15 Unit 3 automatic depressurization system safety relief valves (SRVs) with Buna-N material on October 31 and November 1 Unit

2 DC grounds in the drywell on November 5 and 6 'A'
ESW supply pipe flow on November 20 The inspectors selected these issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the
OD s to assess whether

TS operability was properly justified and the subject component or

system remained available such that no unrecognized increase in risk occurred. The

inspectors compared the operability and design criteria in the appropriate sections of the

TS s and
UFSAR to
PBA [[]]

PS's evaluations to determine whether the components or systems were operable. Where compensatory measures were required to maintain

operability, the inspectors determined whether the measures in place would function as

intended and were properly controlled by

PBA [[]]

PS. The inspectors determined, where

appropriate, compliance with bounding limitations associated with the evaluations.

b. Findings No findings were identified.

Enclosure 1R19 Post-Maintenance Testing (71111.19 - 6 samples) a. Inspection Scope The inspectors reviewed the post-maintenance tests (PMTs) for the maintenance

activities listed below to verify that procedures and test activities ensured system operability and functional capability. The inspectors reviewed the test procedure to

verify that the procedure adequately tested the safety functions that may have been affected by the maintenance activity, that the acceptance criteria in the procedure was consistent with the information in the applicable licensing basis and/or design basis

documents (DBDs), and that the procedure had been properly reviewed and approved. The inspectors also witnessed the test or reviewed test data to verify that the test results

adequately demonstrated restoration of the affected safety functions. Unit

2 SRV actuator functional as-left testing on September 27 Unit 2 E-22 bus logic testing on October 2 Unit 2 main steam isolation valve (
MSIV ) as-left stroke timing on October 9 Motor driven fire pump operability test following maintenance on November 7 Unit
2 APRM functional test following trouble-shooting on November 30 E-1

EDG Surveillance Test (ST) following maintenance on December 3 b. Findings

No findings were identified.

1R20 Refueling Outage (71111.20 - 1 sample) a. Inspection Scope The Unit

2 RFO (P2R19) was conducted from September 9, 2012 through October 18, 2012. During this inspection period, the inspectors performed the activities listed below to verify

PBAPS's controls of outage activities:

Configuration management, including maintenance of defense-in-depth, commensurate with the outage plan for the key safety functions and compliance with the applicable

TS s when taking equipment
OOS [[Implementation of clearance activities and confirmation that tags were properly hung and that equipment was appropriately configured to safely support the associated work or testing Installation and configuration of reactor coolant pressure, level, and temperature instrumentation instruments to provide accurate indication and instrument error accounting Status and configuration of electrical systems and switchyard activities to ensure that]]
TS s were met Monitoring of decay heat removal operations Impact of outage work on the sustained operation of the spent fuel pool (

SFP) cooling system Reactor water inventory controls, including flow paths, alternative means for water inventory additions, and controls to prevent unexpected inventory changes Maintenance of secondary containment as required by TSs

Enclosure Core verification - independently reviewed selected portions of core verification activities and reactor physics testing Torus closure - conducted a thorough walkdown of accessible torus areas above the suppression pool water line prior to reactor startup to verify that all debris, tools, and diving gear were removed Drywell closure - conducted a thorough inspection and walkdown of the primary containment prior to reactor startup to identify any remaining debris, tools, and equipment were removed prior to reactor startup Reactor startup preparations - reviewed the tracking of startup prerequisites and observed the Plant Operations Review Committee meeting on October 15, 2012, to ensure outstanding outage issues were resolved, and startup reviews were detailed Startup and ascension to full power operation - observed selected activities including: reactor criticality; portions of the plant heat-up, main generator synchronization to the grid, and portions of the power ascension to full power

operation Licensee identification and resolution of problems - reviewed corrective action reports related to

RFO and startup activities to verify that

PBAPS was identifying issues at the appropriate level and taking adequate corrective action to resolve the

issues b. Findings

No findings were identified. 1R22 Surveillance Testing (71111.22 - 5 samples) a. Inspection Scope (4 routine surveillances;

1 RCS sample) The inspectors observed performance of

STs and/or reviewed test data of selected risk-

significant

SSC s to assess whether test results satisfied
TS s, the
UFSAR , and

PBAPS

procedure requirements. The inspectors verified that test acceptance criteria were clear, tests demonstrated operational readiness and were consistent with design documentation, test instrumentation had current calibrations and the range and accuracy

for the application, tests were performed as written, and applicable test prerequisites

were satisfied. Upon test completion, the inspectors considered whether the test results

supported that equipment was capable of performing the required safety functions. The inspectors reviewed the following

ST s:
ST -M-57B-744-2, Unit 2D 125/250 Volts
DC Battery Service Test, on October 1
ST -O-054-754-2, E42
4KV Bus Undervoltage Relays and
LOCA /LOOP Functional Test and E42 and E424 Alternate Shutdown Control Functional Test on October 4
ST -O-080-675-2, Reactor Pressure Vessel (
ASME Class I) Leakage Pressure Test, on October 15 and 16, 2012
ST -O-023-301-2, High-Pressure Coolant Injection (
HPCI ) Pump, Valve, Flow and Unit Cooler Functional and In-Service Test, on October 19
ST -O-020-560-2(3), Reactor Coolant Leakage Test, various tests from October 1 through December 31, 2012 (

RCS leakage sample)

b. Findings

No findings were identified.

Enclosure Cornerstone: Emergency Preparedness

1EP 6

EP Drill Evaluation (71114.06 - 1 sample)

Simulator Evaluation a. Inspection Scope The inspectors evaluated the conduct of a routine

PBA [[]]

PS emergency drill on

December 12, 2012, to identify any weaknesses and deficiencies in the classification,

notification, and protective action recommendation development activities. The

inspectors observed emergency response operations in the simulator, and technical support center to determine whether the event classification, notifications, and protective action recommendations were performed in accordance with procedures. The

inspectors also attended the control room simulator drill critique to compare inspector

observations with those identified by

PBAPS staff in order to evaluate

PBAPS's critique

and to verify whether

PBA [[]]

PS staff was properly identifying weaknesses and entering

them into the CAP. b. Findings

No findings were identified.

2.

RADIAT [[]]
ION [[]]
SAFE [[]]

TY

Cornerstone: Occupational/Public Radiation Safety (PS) 2RS5 Radiation Monitoring Instrumentation (71124.05) a. Inspection Scope During the week of December 3 - 7, 2012, the inspectors verified that Exelon personnel

were ensuring the accuracy and operability of radiation monitoring instruments that are

used to (1) monitor areas, materials, and workers to ensure a radiological safe work environment, and (2) detect and quantify radioactive process streams and effluent releases. The instrumentation subject to this review included equipment used to monitor

radiological conditions incident to normal plant operations, including anticipated

operational occurrences, and conditions resulting from postulated accidents. The

inspectors used the requirements in

10 CFR Part 20, 10
CFR Part 50 Appendix A - Criterion 60, "Control of Release of Radioactivity to the Environment," and Criterion 64, "Monitoring Radioactive Releases,"
10 CFR 50 Appendix I, "Numerical Guides for Design Objectives and Limiting Conditions for Operation to meet the Criterion "As Low as is Reasonably Achievable" (

ALARA) for Radioactive Material in Light-Water - Cooled Nuclear Power Reactor Effluents," 40 CFR Part 190, "Environmental Radiation

Protection Standards for Nuclear Power Operations,"

NUREG -0737, "Clarification of Three Mile Island Corrective Action Requirements," Offsite Dose Calculation Manual (
ODCM ),
TS s, applicable industry standards, and Exelon's procedures required by

TSs

as criteria for determining compliance.

Enclosure The inspectors performed plant walkdowns of effluent radiation monitoring systems, including liquid and gaseous systems. The inspectors verified that effluent/process monitor configurations align with

OD [[]]

CM descriptions. The inspectors verified that channel calibration and functional tests were performed

consistent with radiological effluent

TS s (

RETS)/ODCM. The inspectors verified that (a) Exelon calibrated its monitors with National Institute of Standards and Technology

(NIST) traceable sources, (b) if a primary calibration, it adequately represents the plant nuclide mix, (c) if a secondary calibration, it verifies the primary calibration, and (d) the channel calibrations encompass the instrument's alarm set points. The inspectors verified that effluent monitor alarm set points were established as

provided in the

OD [[]]

CM and station procedures. For changes to effluent monitor set points, the inspectors evaluated the basis for changes to ensure that an adequate justification exists. The inspectors selected laboratory analytical instruments used for radiological analyses

and verified that daily performance checks and calibration data indicated that the

frequency of the calibrations was adequate and there were no indications of degraded instrument performance. As part of the problem identification and resolution (PI&R) review, the inspectors verified

that appropriate corrective actions were implemented in response to indications of

degraded instrument performance. The inspectors selected the drywell/containment high-range monitor and reviewed the

calibration documentation since the last inspection. The inspectors verified that an electronic calibration was completed for all range decades above 10 rem/hour and that at least one decade at or below 10 rem/hour was calibrated using an appropriate radiation source. The inspectors determined that the calibration acceptance criteria were reasonable,

accounting for the large measuring range and the intended purpose of the instruments. The inspectors reviewed Exelon's capability to collect high-range, post-accident iodine effluent samples. The inspectors observed electronic and radiation calibration of these instruments to

verify conformity with Exelon's calibration and test protocols. The inspectors reviewed Exelon's 10 CFR Part 61, "Licensing Requirements for Land

Disposal of Radioactive Waste," source term to determine if the calibration sources used

were representative of the types and energies of radiation encountered in the plant. The inspectors verified that problems associated with radiation monitoring instrumentation were being identified by Exelon personnel at an appropriate threshold and were properly addressed for resolution in Exelon's CAP.

Enclosure b. Findings No findings were identified. 2RS6 Radioactive Gaseous and Liquid Effluent Treatment (71124.06 - 1 sample) a. Inspection Scope During the week of December 3 - 7, 2012, the inspectors: (1) ensured that the gaseous and liquid effluent processing systems were maintained so that radiological discharges are properly mitigated, monitored, and evaluated with regard to public exposure;

(2) ensured that abnormal radioactive gaseous or liquid discharges and conditions, when

effluent radiation monitors were OOS, were controlled in accordance with applicable

regulatory requirements and Exelon procedures; (3) verified that Exelon's quality control program ensured that the radioactive effluent sampling and analysis requirements were satisfied so that discharges of radioactive materials were adequately quantified and

evaluated; and (4) verified the adequacy of public dose calculations and projections

resulting from radioactive effluent discharges. The inspectors used the requirements in

CFR Part 20; 10
CFR 50.35(a)
TS s; 10

CFR Part 50 Appendix A - Criterion 60,

"Control of Release of Radioactivity to the Environment," and Criterion 64, "Monitoring Radioactive Releases;

10 CFR 50 Appendix I Numerical Guides for Design Objectives and Limiting Conditions for Operations to Meet the Criterion "

ALARA" for Radioactive

Material in Light-Water - Cooled Nuclear Power Reactor Effluents;" 10 CFR 50.75(g),

"Reporting and Recordkeeping for Decommissioning Planning;" 40 CFR Part 141,

"Maximum Contaminant Levels for Radionuclides;"

40 CFR Part 190, "Environmental Radiation Protection Standards for Nuclear Power Operations;" the guidance in Regulatory Guides 1.109, 1.21, 4.1 and 4.15;
NUREG -1301 or
1302 OD [[]]

CM Guidance:

Standard Radiological Effluent Control, as well as applicable Industry standards, and

Exelon procedures required by

TS s/

ODCM as criteria for determining compliance. The inspectors reviewed the Annual Radiological Effluent Release Reports issued since the last inspection. The inspectors determined that the reports were submitted as

required by the

ODCM /

TSs. The inspectors identified radioactive effluent monitor operability issues reported by Exelon as provided in effluent release reports, and

determined that the issues were entered into the

CAP and adequately resolved. The inspectors reviewed changes to the

ODCM made by Exelon since the last inspection. The inspectors determined that Exelon had not identified any non-

radioactive systems that had become contaminated as disclosed either through an event report or as documented in the

OD [[]]

CM since the last inspection. The inspectors reviewed reported groundwater monitoring results, and changes to Exelon's written program for identifying and controlling contaminated spills/leaks to

groundwater. The inspectors reviewed licensee event reports (LERs) and/or special reports related to

the effluent program issued since the previous inspection. The inspectors identified no additional focus areas for the inspection based on the scope/breadth of problems described in these reports. The inspectors reviewed effluent program implementing

procedures, particularly those associated with effluent sampling, effluent monitor set

point determinations and dose calculations.

Enclosure The inspectors performed walkdowns of selected components of the gaseous and liquid discharge systems to verify that equipment configuration and flow paths align with the documents reviewed and assess equipment material condition. For equipment or areas associated with the systems selected above, that were not readily accessible due to radiological conditions, the inspectors reviewed Exelon's material condition surveillance

records. The inspectors walked down those filtered ventilation systems whose test

results were reviewed during the inspection. The inspectors verified that there were no

conditions, such as degraded high efficiency particulate air (HEPA)/charcoal banks, improper alignment, or system installation issues that would impact the performance, or the effluent monitoring capability, of the effluent system. The inspectors determined that Exelon had not made any significant changes to their

effluent release points. The inspectors observed the routine processing and discharge of effluents (including

sample collection and analysis). The inspectors verified that appropriate effluent

treatment equipment was being used and that radioactive liquid waste was being

processed and discharged in accordance with procedure requirements and aligns with

discharge permits. The inspectors selected effluent sampling activities and verified that adequate controls

had been implemented to ensure representative samples were obtained. The inspectors

determined that the facility was not routinely relying on the use of compensatory

sampling in lieu of adequate system maintenance, based on the frequency of compensatory sampling since the last inspection. The inspectors reviewed the results of the inter-laboratory comparison program to verify

the quality of the radioactive effluent sample analyses. The inspectors verified that the

inter-laboratory comparison program included hard-to-detect isotopes as appropriate. The inspectors reviewed the methodology that Exelon uses to determine the effluent

stack and vent flow rates. The inspectors verified that the flow rates are consistent with

RETS /
ODCM or
UFS [[]]

AR values, and that differences between assumed and actual stack

and vent flow rates do not affect the results of the projected public doses. The inspectors verified that surveillance test results since the previous inspection for

TS required ventilation effluent discharge systems (

HEPA and charcoal filtration) met TS acceptance criteria. The inspectors reviewed radioactive liquid and gaseous waste discharge permits. The inspectors verified that the projected doses to members of the public were accurate and based on representative samples of the discharge path. The inspectors evaluated the

methods used to determine the isotopes that are included in the source term to ensure

all applicable radionuclides were included, within delectability standards. The inspectors

reviewed the current 10 CFR Part 61 analyses to ensure hard-to-detect radionuclides

were included in the source term. The inspectors reviewed changes in

PBA [[]]

PS's offsite dose calculations since the last

inspection. The inspectors verified that the changes are consistent with the

OD [[]]

CM and

Regulatory Guide 1.109. The inspectors reviewed meteorological dispersion and

deposition factors used in the

OD [[]]

CM and effluent dose calculations to ensure appropriate factors were being used for public dose calculations. The inspectors

Enclosure reviewed the latest land use census and verified that changes have been factored into the dose calculations. The inspectors verified that Exelon was continuing to implement the voluntary Nuclear

Energy Institute (NEI)/Industry Groundwater Protection Initiative (GPI) since the last

inspection. The inspectors reviewed monitoring results of the GPI to determine if Exelon

had implemented its program as intended, and to identify any anomalous results. No

anomalous results were identified. The inspectors reviewed identified leakage or spill events and entries made into

CFR 50.75 (g) records. The inspectors reviewed evaluations of leaks or spills, and

reviewed any remediation actions taken for effectiveness. The inspectors reviewed

onsite contamination events involving contamination of groundwater. The inspectors verified that on-site groundwater sample results and a description of any

significant on-site leaks/spills into groundwater for each calendar year were documented in the Annual Radiological Environmental Operating Report for

REMP or the Annual Radiological Effluent Release Report for the radiological effluent

TS (RETS). The inspectors verified that problems associated with the effluent monitoring and control program were being identified by Exelon at an appropriate threshold and were properly

addressed for resolution in Exelon's CAP.

b. Findings No findings were identified.

4.

OTHER [[]]

ACTIVITIES 4OA1 Performance Indicator Verification (71151 - 12 samples)

.1 Mitigating Systems Performance Index (10

MS [[]]

PI samples)

a. Inspection Scope The inspectors sampled

PBAPS 's submittals of the Mitigating Systems Performance Index (

MSPI) for the following systems for the period of October 1, 2011 through

September 30, 2012:

Unit 2 and Unit 3 Emergency Alternating Current Power System (MS06) Unit 2 and Unit

3 HPCI System (
MS 07) Unit 2 and Unit
3 RCIC System (
MS 08) Unit 2 and Unit
3 RHR System (

MS09) Unit 2 and Unit 3 Support Cooling Water System (MS10) To determine the accuracy of the performance indicator (PI) data reported during this

period, the inspectors used definitions and guidance contained in NEI Document 99-02,

"Regulatory Assessment

PI Guideline," Revision 6. The inspectors also reviewed
PBAPS operator narrative logs,
CR s,
MSPI derivation reports, event reports, and

NRC

integrated inspection reports to validate the accuracy of the submittals.

Enclosure b. Findings No findings were identified. .2 Occupational Radiation Safety Cornerstone (1 sample)

a. Inspection Scope The inspectors reviewed a listing of licensee action reports for issues related to the occupational radiation safety

PI (

OR01), which measures non-conformances with high radiation areas greater than 1 Roentgen/hour (R/hr) and unplanned personnel

exposures greater than 100 millirem (mrem) total effective dose equivalent (TEDE), 5 rem skin dose equivalent (SDE), 1.5 rem lens dose equivalent (LDE), or 100 mrem to the unborn child. The inspectors determined that no PI events for occupational radiation safety had occurred during the assessment period.

b. Findings No findings were identified. .3 Public Radiation Safety Cornerstone (1 sample)

a. Inspection Scope The inspectors reviewed a listing of licensee action reports for issues related to the public radiation safety

PI (

PR01), which measures radiological effluent release

occurrences per site that exceed 1.5 mrem/quarter (qtr) whole body or 5 mrem/qtr organ dose for liquid effluents; or 5 millirads (mrads)/qtr gamma air dose, 10 mrads/qtr beta air

dose; or 7.5 mrems/qtr organ doses from Iodine-131, I-133, Hydrogen-3, and particulates for gaseous effluents. The inspectors determined that no PI events for public radiation safety had occurred during the assessment period.

b. Findings No findings were identified. 4OA2 Identification and Resolution of Problems (71152 - 1 sample)

Routine Review of PI&R Activities a. Inspection Scope

As required by Inspection Procedure (IP) 71152, "Promblem Identification and

Resolution," the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that

PBAPS entered issues into the

CAP at an

appropriate threshold, gave adequate attention to timely corrective actions, and identified and addressed adverse trends. In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the

CAP and periodically attended

CR screening meetings.

Enclosure b. Findings and Observations No findings were identified.

.2 Semi-Annual Review to Identify Trends (1 Semi-annual Trend sample)

a. Inspection Scope The inspectors performed a semi-annual review of site issues, as required by Inspection

Procedure 71152, "Problem Identification and Resolution," to identify trends that might

indicate the existence of more significant safety issues. In this review, the inspectors

included repetitive or closely-related issues that may have been documented by Exelon outside of the corrective action program, such as trend reports, performance indicators, major equipment problem lists, system health reports, maintenance rule assessments, and maintenance or corrective action program backlogs. The inspectors also reviewed

Exelon's corrective action program database to assess CRs written in various subject

areas (equipment problems, human performance issues, etc.), as well as individual

issues identified during the

NRC s daily condition report review (Section 4
OA 2.1). The inspectors reviewed 9,048 issue reports (IR) that
PBAPS initiated and entered into the
CAP action tracking system (Passport) from June 1, 2012 through November 30, 2012. The inspectors evaluated the
IR s against the requirements of Exelon
CAP procedure,
LS -
AA -125, and
10 CFR 50, Appendix B, Criterion
XVI , "Corrective Action." b. Findings and Observations No findings were identified. The inspectors determined that
PBAPS was appropriately identifying and entering issues into the
CAP , adequately evaluating the identified issues, and properly identifying adverse trends before they became more safety significant problems. The inspectors noted adverse trends identified by
PBA [[]]

PS in the Maintenance and

Operations Department in the area of human performance; including configuration control and clearance and tagging that have resulted in low-level issues of minor risk significance: Operations - Common Cause Analysis 1419073, "Nuclear Oversight Identified: Operations Shortfalls in Use of Human Performance Tools" - Common Cause Analysis 1423654, "Adverse Trend in Clearance and Tagging Events" -

IR 1430391, "Declining Trend in Site Configuration Control" -
IR 1430644, "Corporate Escalation due to Continued Adverse Human Performance Event Trend" Maintenance -
IR 1425757, "Nuclear Oversight Identified: Lapses in Work Standards Results in Adverse Trend" -

IR 1430748, "Elevation for Maintenance Department Human Performance at Peach Bottom"

Enclosure - Common Cause Analysis 1394685, "Adverse Trend in Maintenance Department and Crew Clock Resets" - Common Cause Analysis 1436530, "Safety and Human Error Prevention Tools Declining Trend in Maintenance"

4OA 3 Follow-up of Events and Notices of Enforcement Discretion (71153 - 4 samples) .1 (Closed)

LER 05000277/2012001-00, Laboratory Analysis Identified Safety Relief Valve and Safety Valve Setpoint Deficiencies (1 sample) On September 25, 2012, site engineering personnel determined, based on information

received from a vendor laboratory performing

SRV / safety valve (
SV ) as-found testing, that
SRV /
SV the open lift setpoint deficiencies existed with six
SRV s and one

SV that

were in place during the 19th Unit 2 operating cycle. The

SRV s /
SV were determined to have their as-found opening setpoints outside of the
TS allowable + 1% tolerance. The six
SRV s outside of their
TS allowable setpoint range were within the

ASME Code

allowable + 3% tolerance. The one

SV outside of its
TS allowable setpoint range also exceeded the
ASME Code allowable + 3% tolerance. The cause of the
SRV s /SV being outside of their allowable as-found setpoints is due to setpoint drift. The
SRV s /

SV were

replaced with refurbished

SRV s /
SV for the 20th Unit 2 operating cycle. There was no actual safety consequences associated with this event. The enforcement aspects of this
LER are discussed in Section 4

OA7. This LER is closed.

.2 (Closed)

LER 05000277/2012002-00, Common Cause Inoperability of Reactor Protection System Turbine Control Valve Instruments (1 sample) On October 1, 2012, during surveillance testing performed during the P2R19

RFO,

Instrumentation and Controls personnel identified that two of the four instruments used

to perform the

RPS scram and end-of-cycle recirculation pump trip (

EOC-RPT) functions

for turbine control valve (TCV) fast closure were outside of their

TS [[allowable value of > 500 psig oil pressure. The 'A' pressure sensing instrument (]]

PS-4121A) was found at a trip setting of 495 psig and the 'B' pressure sensing instrument (PS-4121B) was found at

a trip setting of 493 psig. The cause of this event is due to instrument drift. This

occurrence is reportable as a result of a common cause inoperability that resulted in two

instruments drifting low outside of the TS allowable value. The 'A' and 'B' instruments

were replaced and calibrated to within acceptable limits. There was no actual safety consequences associated with this event. If an operational transient would have occurred during power operations, the 'C' and 'D' instrument channels were operable

and would have provided the

RPS scram and
EOC -RPT trip functions. The enforcement aspects of this
LER are discussed in Section 4
OA 7. This
LER is closed. .3 (Closed)
LER 05000278/2012003-00, Loss of Control Room Emergency Ventilation Function Due to Failure of Ventilation Fan to Start (1 sample) On October 4, 2012, during surveillance testing of a
4KV emergency bus, the 'A'

MCR

emergency ventilation (MCREV) fan did not start as expected when an initiation signal

was generated. Although the 'B'

MCREV fan started per design, the bus that powers the 'B' train of
MCREV was considered inoperable due to planned testing.
PBAPS determined that the cause of this event was that the 'A'

MCREV fan switch was

positioned such that the switch contacts were still open, thereby preventing a start of the

'A' fan.

PBA [[]]

PS determined this event was reportable because it could have prevented

the fulfillment of the

MCR [[]]

EV safety function with both trains inoperable simultaneously.

Enclosure The switch was correctly repositioned on the same day, and the system was returned to an operable status.

PBAPS entered this item into the
CAP for investigation, extent-of-condition review, and evaluation for any additional corrective action that may be required. No findings or violations of
NRC requirements were identified because

TS

allowed outage times were not exceeded. This LER is closed.

.4 Event Response - Super Storm Sandy (1 sample) a. Inspection Scope From October 25 to October 28, 2012, the inspectors reviewed

PBA [[]]

PS's activities to

prepare for the potential arrival of Super Storm Sandy.

PBA [[]]

PS personnel implemented

the actions specified by procedure

OP -
PB -108-111-1001, "Preparation for Severe Weather." On October 29, 2012, inspectors responded to
PBA [[]]

PS due to the expected arrival of Super Storm Sandy within the next 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Inspectors remained on-site

continuously until the passing of the Super Storm on the following day. The inspectors

noted that

PBAPS had staffed the Outage Control Center (

OCC) on October 29, 2012,

to track Super Storm Sandy and provide a centralized location for control of severe

weather-related actions. The inspectors monitored plant activities in the

MCR and the

OCC and monitored selected plant parameters, including: actual and projected onsite weather conditions; offsite power status; key safety equipment status; river water intake

conditions; plant equipment issues; security readiness and equipment issues; and

emergency planning considerations. b. Findings

No findings were identified.

4OA 5 Other Activities .1 Institute of Nuclear Power Operations (

INPO) Report Review

a. Inspection Scope The inspectors reviewed the final report for the

PBAPS [[]]
INPO assessment conducted in April 2012. The inspectors reviewed this report to ensure that any issues identified were consistent with
NRC perspectives of
PBAPS performance and to determine if
IN [[]]

PO

identified any significant safety issues that required further NRC follow-up. b. Findings No findings were identified.

.2 Temporary Instruction (TI) 2515/182, Review of the Industry Initiative to Control Degradation of Underground Piping and Tanks, Phase 1 (2515/182 - 1 sample) a. Inspection Scope Exelon's buried piping and underground piping and tanks program was inspected in

accordance with paragraphs 03.01a through 03.01c of the TI and was found to meet all

applicable aspects of the

NEI document 09-14, Revision 1, as set forth in Table 1 of the

TI 2515/182.

Enclosure b. Findings No findings were identified. .3

TI 2515/185 Follow-up on the Industry's

GPI

a. Inspection Scope The objective of this TI is to assess groundwater protection programs to determine

whether licensees' have implemented the program elements in their groundwater protection programs that were identified as incomplete in

TI 2515/173. During December 3 - 7, 2012, the inspectors reviewed previously identified incomplete program elements within Exelon's Industry

GPI. The incomplete program elements

previously identified (NRC Inspection Report 05000277/2010004: 05000278/2010004) were: 1.

GPI Objective 1.2 g - At the time of the inspection, a specific frequency had been established for periodic reviews of

SSCs and work practices. However, the frequency had not yet been placed in a procedure. This matter was identified in a

self-assessment and placed in the

CAP. (

AR924237) 2. GPI Objective 1.3 f - At the time of the inspection, Exelon had established a program for the preventative maintenance of groundwater wells. However, the program had not yet been incorporated into all applicable implementing procedures. Exelon

placed this issue into its

CAP. (

AR924237) 3. GPI Objective 1.4 a.- At the time of the inspection, written procedures had not been established outlining the decision making process for remediation of leaks or spills or other instances of inadvertent releases, including consideration of migration

pathways. Exelon identified this issue during an assessment of

GPI implementation and placed this issue into its

CAP. (AR924237) 4. GPI Objective 1.4 c.- At the time of the inspection, an evaluation had not been performed and documented on the decommissioning impacts resulting from remediation activities or the absence thereof (e.g., do licensee procedures include a

decision making process to evaluate prompt remediation or delayed remediation and its impact on decommissioning). Exelon identified this issue during an assessment of

GPI implementation and placed this issue into its
CAP. (AR924237) 5.
GPI Objective 1.5 - Exelon developed program procedures to establish a record keeping program to meet the requirements of 10

CFR 50.75(g) and developed an

historical spill/leak list. However, Exelon identified, during a June 2010 audit, that

the individual record files did not reflect some information contained in station files.

Exelon initiated a review to ensure all appropriate information, consistent with criteria in

10 CFR 50.75(g) and the program procedure, were included in its decommissioning files. Exelon placed this matter into its
CAP. (AR1081998) 6.
GPI Objective 3.2 a. - An independent, knowledgeable individual had not performed, under the auspices of

NEI, an initial review within one year of the initial self-

Enclosure assessment, per

GPI Objective 3.1.a. This assessment was completed on February 28, 2010. Exelon placed this matter into its

CAP. (AR1041430) The inspectors reviewed actions taken to correct the above listed incomplete items:

b. Findings and Observations

No findings were identified. The inspectors concluded that Exelon had satisfactorily addressed the incomplete items

documented in TI 2515/173 as discussed below.

Item 1: Exelon inserted in section 4.3.2 of Procedure

EN -
AA -408-4000 the frequency for reviewing and updating the risk associated with
SSC s. Item 2: Exelon inserted in section 4.1.3.3 of Procedure

EN-AA-408-4000 a groundwater

well preventative maintenance program; For incomplete item 3, Exelon inserted in

section 4.1.7 of Procedure

EN -
AA -408-4000 and Attachment 2 of Procedure
EN -

AA-407

the decision making process for the remediation of leaks or spills. Item 3: Exelon inserted in section 4.1.7 of Procedure

EN -

AA-408-4000 and Attachment

of Procedure

EN -

AA-407 the decision making process for the remediation of leaks or

spills.

Item 4: Exelon inserted in section 4.1.7 of Procedure

EN -

AA-408-4000, and created with an Operational Technical Decision, a methodology for evaluating decommissioning impacts resulting from groundwater remediation activities.

Item 5: Exelon amended Procedure

RP -
AA -228 (Revision 1) to ensure adequate records are maintained to meet the requirements of 10 CFR 50.75(g). The inspectors noted that this issue was associated with Exelon's Three Mile Island site and not
PBA [[]]

PS.

Item 6: Although the independent assessment was not performed in the time frame

specified in the

NEI letter, as noted in

NRC Inspection Report 05000277/2010004: 05000278/2010004, this assessment was completed on February 28, 2010, and no further action is necessary.

.4 TI 2515/187 - Inspection of Near-Term Task Force Recommendation 2.3 - Flooding Walkdowns

a. Inspection Scope The inspectors verified that

PBA [[]]

PS's walkdown packages for both the accompanied and

independent plant area walkdowns listed below contained the elements as specified in NEI 12-07 Walkdown Guidance document.

Enclosure The inspectors accompanied

PBAPS and contracted personnel on their flooding walkdowns of the following plant areas: E-1
EDG room E-2
EDG room E-3
EDG room E-4
EDG room
EDG cardox and
ESW booster pump room The inspectors verified that
PBAPS [[confirmed the following flood protection features: Visual inspection of the flood protection feature was performed if the flood protection feature was relevant. External visual inspection for indications of degradation that would prevent its credited function from being performed. Reasonable simulation of manual flood protection actions. Critical]]
SSC [[dimensions were measured. Available physical margin, where applicable, was determined. Flood protection feature functionality was determined using both visual observation and documentation review. The inspectors independently walked down the safety-related pump structure, and verified that the following flood protection features were in place: Penetration seals Flood doors and gaskets Internal and external walls Floor Roof parapet and drains Sump system Reasonable simulation of manual flood protection actions The inspectors verified that noncompliances with current licensing requirements, and issues identified in accordance with the 10]]
CFR 50.54(f) letter, Item 2.g of Enclosure 4, were entered into
PBAP 's
CAP. In addition, issues identified in response to Item 2.g that could challenge risk significant equipment and
PBA [[]]

PS's ability to mitigate the

consequences will be subject to additional NRC evaluation.

.5

TI 2515/188 - Inspection of Near-Term Task Force Recommendation 2.3 - Seismic Walkdowns a. Inspection Scope The inspectors accompanied

PBAPS and contracted personnel on their seismic

walkdowns of selected portions of the following plant areas: Safety-related pump structure Service water traveling screen structure The inspectors observed walkdowns of the following equipment listed on the

PBAPS seismic walkdown equipment list (

SWEL):

Enclosure

MO -2-30-2233A, Unit 2 'A' sluice gate 2
CP 042, Unit 2 'C'
HPSW pump P0D-2-40H-20223-3, Unit 2
HPSW pump room outside air supply damper P0D-2-40H-20223-4, Unit
2 HPSW pump room exhaust return to room damper
DPS 30224-4, Unit
2 HPSW pump room
DP sensor
2AV 060, Unit 2
HPSW pump room air supply fan 'A' The inspectors independently performed their walkdown of the Unit 2 drywell on September 30 and October 12, 2012, and the following equipment listed on the
PBAPS seismic walkdown equipment list (
SWEL ):
2GT 545, 'G'
ADS instrument nitrogen accumulator
2KT 545, 'K'
ADS instrument nitrogen accumulator The inspectors verified that, for the equipment listed above, the
PBA [[]]

PS and contracted

personnel confirmed that the following seismic features were free of potential adverse seismic conditions: Anchorage was free of bent, broken, missing, or loose hardware Anchorage was free of corrosion that is more than mild surface oxidation Anchorage was free of visible cracks in the concrete near the anchors Anchorage configuration was consistent with plant documentation SSCs will not be damaged from impact by nearby equipment or structures Overhead equipment, distribution systems, ceiling tiles and lighting, and masonry block walls are secure and not likely to collapse onto the equipment Attached lines have adequate flexibility to avoid damage The area appears to be free of potentially adverse seismic interactions that could cause flooding or spray in the area The area appears to be free of potentially adverse seismic interactions that could cause a fire in the area The area appears to be free of potentially adverse seismic interactions associated with housekeeping practices, storage of portable equipment, and temporary installations (e.g., scaffolding, lead shielding) Observations made during the walkdown that could not be determined to be acceptable

were entered into

PBAPS 's
CAP for evaluation. Additionally, inspectors verified that
PBAPS did not identify any items that could allow the
SFP to drain down rapidly; therefore, no such items were added to the
SWEL for a walkdown by

PBAPS personnel.

b. Findings

No findings were identified. .6 Post-Approval Site Inspection for License Renewal (IP 71003)

a. Inspection Scope On a sampling basis, the inspectors verified that Exelon had completed the necessary actions to comply with the license conditions that are a part of the renewed operating

Enclosure license, and had implemented the aging management programs included in the

NRC staff's license renewal safety evaluation report. The inspectors verified that Exelon followed the guidance in

NEI 99-04 for the license renewal commitment change process, including the elimination of commitments, and properly evaluated, and reported where

necessary, changes to license renewal commitments listed in the

UFS [[]]

AR in accordance

with 10 CFR 50.59.

This inspection verified, by observation, selected: License conditions added as part of the

PBAPS renewed license License renewal commitments and selected aging management programs License renewal commitments revised after the renewed license was granted, were implemented in accordance with Title 10 of the Code of Federal Regulations (

CFR) Part 54, "Requirements for the Renewal of Operating Licenses for Nuclear Power

Plants"

b. Findings and Observations No findings were identified.

The inspectors concluded that Exelon's actions regarding the commitments described

below were complete and met regulatory expectations as reflected in the NRC staff's

safety evaluation report. Commitments and Aging Management Programs Flow-Accelerated Corrosion Program The inspectors observed ultrasonic measurements taken of the standby liquid control tank suction piping (WO CO241697). The piping was examined 12-inches on either side

of the weld between valve HV-2-11-11 and the tee downstream of the weld location.

The examination was implemented in accordance with procedure

ER -

AA-335-045, "Manual Ultrasonic Requirements for Non-PDI Examinations," Revision 2. This evolution was evidence of the implementation of the aging management program proposed in the original Exelon license renewal application Section B.1.1, "Flow-Accelerated Corrosion

Program," which was codified by the renewed license condition requiring renewal related aging management programs entered into the

UFS [[]]

AR.

Commitment 6 - Inspection of Outer Sluice Gates Commitment 6, in the renewal Safety Evaluation Report, Appendix A, requires Exelon to

perform an inspection of outer sluice gates in the circulating water pump structure. This

commitment encompassed by the

UFS [[]]

AR, Section A.2.5, "Outdoor, Buried, and

Submerged Component Inspection Activities," and must be performed prior to period of extended operation. This commitment was generated in the applicant's response to the

NRC 's request for additional information request (

RAI) 3.5-3, in a letter dated May 21,

2002. This commitment was tracked by Exelon as Commitment T04329, which was

noted on the work order implementing the inspection.

The outer sluice gates work in conjunction with the ESW system to support safe shutdown following a loss of the normal heat sink. As a consequence of the safe shutdown function of the structural steel sluice gates, Exelon identified the structural

Enclosure steel sluice gates and embedment, in Table 2.4-11 of the original application to renew their license, as a long-lived structural component of the circulating water pump structure that is subject to an aging management review. The sluice gates and embedment have the intended function of maintaining the pressure boundary when the emergency cooling

water system is called upon to operate. During the Unit 2 outage, when desilting

operations are implemented at the intakes, the circulating water pump structure, the

ESW cross-tie sluice gate,
ESW and
HP [[]]

SW cross-tie sluice gate, and the Unit 2 'A' and

'B' sluice gates, were visually examined for a significant loss of material. The inspectors observed the diving and inspection activities implemented as part of the desilting operations, interviewed the operation manager, and reviewed the recurring task activity

(WO NBR R1178278).

Commitment 8 - Reactor Pressure Vessel Top Guide Inspection Commitment 8, in the renewal Safety Evaluation Report, Appendix A, requires that

Exelon perform an inspection of the reactor pressure vessel top guide prior to the period

of extended operation. The commitment is part of the aging management program as

described in the

UFSAR , Section A.2.7, "Reactor Pressure Vessel and Internals
ISI Program." This commitment was made in response to an open item 4.5.2-1, in a letter to the
NRC dated January 14, 2003. The

NRC inspectors observed the implementation of remote visual examinations of the reactor pressure vessel top guide and reviewed the

ongoing video interrogation of the guides by trained and knowledgeable vendors.

MR Structure Monitoring Program The inspectors observed the implementation of a visual examination of the structures

associated with the 'B' and 'D' core spray rooms. This inspection was part of aging

management program B1.16, "MR Structure Monitoring Program." The inspectors noted that the check list used during the visual inspection included all the essential elements of a maintenance monitoring program. Such items as corrosion, missing or degraded

grout, and crack welds in structural steel components were included in the checklist.

Masonry walls, although limited, were visual inspected for cracked joints, deteriorated

penetrations, and missing or broken blocks. Component supports were checked for missing or loose bolts and cracked welds.

4OA6 Meetings, Including Exit Quarterly Resident Exit Meeting Summary On January 18, 2013, the resident inspectors presented the inspection results to

Mr. Michael Massaro, Site Vice President, and other

PBA [[]]

PS staff, who acknowledged

the findings. Mr.

M. Gray, Chief,
USNRC , Region 1, Division of Reactor Projects, Branch 4, attended this quarterly inspection exit meeting. The inspectors verified that no proprietary information was retained by the inspectors or documented in this report.
4OA 7 Licensee-Identified Violations The following violations of very low safety significance (Green) were identified by Exelon and are violations of

NRC requirements which meet the criteria of the NRC Enforcement

Policy for being dispositioned as

NCV s.
TS 3.4.3 Limiting Condition for Operation (LCO) requires that 11 of
13 SRV s\

SVs shall be operable in reactor operating modes 1, 2, and 3. TS 3.4.3.1 surveillance

Enclosure requirement states that the

SRV s\
SV s opening lift setpoints are maintained within + 1% tolerance of the design opening pressure. Contrary to the above, information received by site engineering from a laboratory performing
SRV \

SV as-found testing, determined that on September 25, 2012, the valve setpoint deficiencies existed with

six

SRV s and one
SV that were in place during the Unit 2 19 operating cycle. The
SRV s /

SV were determined to have their as-found setpoints outside of the

TS allowable + 1% tolerance. The six
SRV s outside of their
TS allowable setpoint range were within the
ASME Code allowable + 3% tolerance. The one
SV outside of its
TS allowable setpoint range also slightly exceeded the
ASME Code allowable + 3% tolerance at a value of + 3.4%. The cause of the
SRV s /

SV being outside of their

allowable as-found setpoints was due to setpoint drift. The

SRV s /

SV were replaced

with refurbished

SRV s/
SV for the 20th Unit 2 operating cycle. The amount of setpoint drift was within the as found Target Rock
SRV values when compared to industry data. The

SRVs/SV were replaced with refurbished valves that were tested and opened within the allowable + 1% tolerance. The inspectors determined that the finding was of very low safety significance (Green) in accordance with Section A of

Exhibit 2 in Appendix A of IMC 0609, "The Significance Determination Process for

Findings at Power," because the SRV's safety function was not affected. Although

outside the lift setpoint tolerance, the as found

SRV /
SV lift pressure values would not have challenged the reactor vessel design maximum pressure rating during the most limiting postulated accident event. The inspectors reviewed
PBAPS 's planned corrective actions to address the
SRV setpoint drift issue and considered a planned industry standard
TS setpoint change submittal to a + 3% tolerance appropriate. Because this finding is of very low safety significance, the as-found out of tolerance

SRVs were replaced with SRVs that had

the proper lift setpoint prior to the Unit 2 reactor plant startup, and the issue was

entered into Exelon's

CAP under

IR 1418320 and apparent cause evaluation

20516, this violation is being treated as a Green

NCV consistent with the
NRC 's Enforcement Policy.
TS [[]]
LCO 3.3.1.1, Condition B, requires that with one
RPS instrument function with one or more required channels inoperable, action shall be taken within six hours to place a channel or trip system in a trippedcondition within six hours. Additionally,
TS [[]]
LCO 3.3.4.2, Condition A, requires that with one or more required end of cycle (

EOC) recirculation pump trip (RPT) instrument channels inoperable, action be taken to

place the channel in a tripped condition within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> if the channel is not restored

to operable status. Contrary to the above,

PBA [[]]

PS determined that the 'A' and 'B'

channels of the Unit 2 turbine control valve (TCV) fast closure pressure sensing

instruments were inoperable for a period of time greater than allowed by TS. Specifically, the as-found trip setpoints of the 'A' and 'B' sensing instruments were identified to be below the allowable trip setting during surveillance testing on October

1, 2012.

PBAPS Unit 2 was defueled to support the 19th

RFO during performance of the ST. Both instruments were replaced and calibrated to within acceptable limits

prior to reactor startup. The inspectors determined that the finding was of very low safety significance (Green) in accordance with Section C of Exhibit 2 in Appendix A of IMC 0609, " The Significance Determination Process for Findings at Power,"

because RPS system trip capability was maintained with the 'C' and 'D' instrument

channels. Because this finding is of very low safety significance and has been

entered into Exelon's

CAP under
IR 1421069, this violation is being treated as a Green
NCV consistent with the

NRC Enforcement Policy.

Enclosure

10 CFR 50.54(q) requires, in part, that a power reactor licensee follow an Emergency Plan that meets the requirements of 10

CFR 50.47(b). 10 CFR 50.47(b) requires, in part, that a standard emergency classification and action level scheme, the bases of

which includes facility system and effluent parameters, is in use by Exelon. Contrary to the above, between December 2008 and November 2012, the standard emergency classification and action level scheme associated with radiological

effluents at

PBA [[]]

PS was not updated to reflect the changes in X/Q dispersion factor

that occurred during the December

2008 OD [[]]

CM revision. Consequently, the effluent

monitor emergency classification and action level thresholds for the reactor building

exhaust vent stack were non-conservative until this condition was identified and promptly corrected by

PBAPS in November 2012. The inspectors determined that the finding was of very low safety significance (Green) in accordance with

NRC IMC

0609, Appendix B, "Emergency Preparedness Significance Determination Process,"

Table 5.4-1, because the emergency action level (EAL) classification process would

not be capable of classifying an Unusual Event (UE) within 15 minutes, but would still be capable of declaring all other

EAL s within 15 minutes. Because this finding is of very low safety significance, and has been entered into Exelon's

CAP under

IR 1439489, this violation is being treated as a Green
NCV consistent with the

NRC's

Enforcement Policy.

ATTACH [[]]
MENT [[:]]
SUPPLE [[]]
MENTAR Y
INFORM [[]]
ATION Attachment
SUPPLE [[]]
MENTAR Y
INFORM [[]]
ATION [[]]
KEY [[]]
POINTS [[]]
OF [[]]

CONTACT Exelon Generation Company Personnel Michael Massaro, Site Vice President

P. Navin, Plant Manager J. Armstrong, Regulatory Assurance Manager T. Moore, Site Engineering Director

M. Herr, Operations Director

J. Kovalchick, Security Manager P. Rau, Work Management Director R. Reiner, Chemistry Manager R. Holmes, Radiation Protection Manager

J. Bowers, Training Director

B. Henningan, Operations Training Manager

NRC Personnel M. Gray, Branch Chief S. Hansell, Senior Resident Inspector

A. Ziedonis, Resident Inspector

T. Burns, Reactor Inspector
J. Furia, Senior Health Physicist M. Modes, Senior Reactor Engineer A. Rosebrook, Senior Project Engineer
LIST [[]]
OF [[]]
ITEMS [[]]
OPENED ,
CLOSED ,
DISCUS [[]]

SED

Opened

None

Opened/Closed None

Closed 05000277/2012001-00 LER Laboratory Analysis Identifies Safety Relief Valve and Safety Valve Setpoint Deficiencies

(Section 4OA3.1)05000277/2012002-00 LER Common Cause Inoperability of

Reactor Protection System Turbine Control Valve Instruments (Section 4OA3.2)

Attachment 05000278/2012003-00 LER Loss of Control Room Emergency Ventilation Function Due to Failure of Ventilation Fan to Start Failure of

Primary Containment

(Section 4OA3.3)

Discussed/Closed None.

LIST [[]]
OF [[]]
DOCUME [[]]
NTS [[]]
REVIEW [[]]

ED * -- Indicates NRC-identified

Section 1R01: Adverse Weather Protection Procedures

RT -I-066-200-2, Heat Trace System Testing, Revision 10, Completed 09/26/12
RT -O-040-620-2, Outbuilding
HVAC and Outer Screen Inspection for Winter Operation, Revision 16, Completed 11/11/12
RT -O-040-630-2, Winterizing Procedure, Revision 12, Completed 11/11/12
MA -
PB -1003, Winter Readiness and Storm Response Guidelines for the Peach Bottom Facility, Revision
8 OP -
AA -108-111-1001, Severe Weather and Natural Disaster Guidelines, Revision 9
OP -
PB -108-111-1001, Preparation for Severe Weather, Revision 9
ARC Number: South 500
KV Sub Station General Alarm ARC-006 00C224 J-5, Revision 2,
PBAPS Alarm Response Card

AO 53.2-0, Equipment Checks After a Thunderstorm, Revision 4

Condition Reports 1432946, Water Intrusion E-2 EDG Bay from Door #D03, Performed on 10/30

1432957, Update to

IR 1431650 for 500

KV CB Trouble Alarm

1197180, 2011-2012 Winter Readiness Tracking Assignments 1244622, 2011-2012 Winter Readiness Tracking Assignments (Snow) 1344584, 2011-2012 Post-Winter Readiness Critique

1355667,

PBA [[]]

PS Winter Readiness Critique for 2011-2012

1304044, Engineering Review Requested

296874,

2AE 052 U2

RB Vent Supply Heating Coil Replacement 1420796, Backdraft Damper did not Auto Close 1420797, Backdraft Damper did not Auto Close

1418459, Insulation Cover Broken off on Penetration "S" on U2 CST

21639, 'A' Auxiliary Boiler Suspected Leakage

1435494, 'A' Auxiliary Boiler Failed Post Maintenance

PMT 1454745, 'A' Auxiliary Boiler Replacement:
B&W Notified

PM of Delivery Date 1429450, 0BE139 Temperature Control not Functioning 1429547, Heating Unit not Working

1431972, Mechanically Restrain Cooling Tower Fans In Accordance With

OP -

PB-108-111-1001

1437802, Unit 2 Change in Reactor Drywell Pressure Indications

1437808, Fan Does Not Start

Attachment 1438614, Test Equipment Prevents Closing Louvers for Winter Readiness 1438884,

TIS -00520-02 Shows Signs of Wire Damage 1442654, Work Week 1247

PMM6 Unable to Complete Scheduled Work 1442663, Work Week 1247 This IR Goes with 1442654

1443988, Nitrogen Leaking from Boilers

1444436,

BRE #3 Wall Heater

OOS

1452161, Wall Heater in BRE 8 is Broken

1444437,

BRE #9 Wall Heater
OOS 1444491,
0AK 019 - Low Condenser Refrigerant Pressure 1444496, 0

AK019 - Low Evaporator Entering Water Temperature

1444518, No Steam or Water at Hand Valve When Placing Steam Hear In Service

1445229, Develop Procedure for MCR Chiller Winter Operation

1445423, Multiple Trips of Ionics Skid 1445515, 2012-2013 Winter Readiness Exception to

WC -

AA-107 Attachment 1 1444626, Potential Asbestos Contamination

1444977, Aux Steam Trap Through Wall Leak D/S HV-3-24F-38349

1445469, Work Not Completed as Scheduled

1446454, Valve Packing Leak RB Heating System

1446572,

0AK 019 Low Condenser Refrigerant Pressure 1447482, 2
BK 018 Low Condenser Refrigerant Pressure 1452170, Abnormal Lineup Required to Keep
RB Negative

DP in Spec

1452736,

HV -2-24F-28426A

RB Heating Coil 2AE053 Drain Valve

1452708,

2BE 052

RB Ventilation Supply Heating Coil 'B'

1453924, Unit

2 RB Face Damper not Modulating 1455467,
TBCCW Head Tank Now Lowering 1456262,
OP -

AA-102-102 Gap Found

1456604, Leaking Steam Trap in Return Line of Area Heater

1457021, Preparation for Discharge Canal to Intake Pond Cross-Tie Gate Removal

1458286, Tracking for

AO 29.2 Miscellaneous

SE-16 Bases, Grid Emergency - Bases, Revision 12, Performed on October 30, 2012

Peach Bottom Certification Letter for Winter Readiness, dated November 15, 2012

Unified Control Room Log, Monday, November 26, 2012, Day Shift

Unified Control Room Log, Thursday, December 13, 2012, Night Shift Unified Control Room Log, Friday, December 14, 2012, Night Shift Unified Control Room Log, Sunday, December 16, 2012, Day Shift

Unified Control Room Log, Monday, December 17, 2012, Night Shift

Unified Control Room Log, Monday, October 29-31, 2012, Day and Night Shifts Section 1R04: Equipment Alignment Procedures

SO 10.1.A-3B

COL, RHR System Setup for Automatic Operation Loop B, Revision 21

Condition Reports *1452357,

MSO Impacted
MCC Not Updated on System Operating Procedure Check Off List
WO s /

ARs 01432946, Water Intrusion E-2 EDG Bay from Door #D03

01429435, Loose Nut Found in E-3 Standby Diesel Generator Room

Attachment

Attachment Section 1R05: Fire Protection

Procedures

PF -10, Unit 3
RB 'B'
RHR Pump and
HX Room, Revision 2
PF -9, Unit 3
RB 'D'
RHR Pump and
HX Room, Revision 2
PF -3, Unit 2
RB 'D'
RHR Pump and
HX Room, Revision 4
PF -5H, Unit 2
RB General Area, North - Elevation 135', Revision 3
PF -5P, Unit 2
RB General Area, South - Elevation 135', Revision
4 PF -136,

ECT, General Area - Elevation 123' and 153', Revision 2

Condition Reports 1448248, Ground Water Intrusion in 2 'D' RHR Room

1443419, Housekeeping Zone #6 Unit 2 RB 135' Walkdown 1443720, Combustible Material in Combustible Free Zone 1446031, No Control for Combustible Material on Rad Waste 135' Elevation

1446039, No Control for Combustible Material on Unit 2 RB 135' Elevation

1450015, Housekeeping Issues in Unit 2 RB

1452738, Cart with Wood Blocks on 135' RB South End

1453765, Transient Combustibles Under Stairwell 1455595, Housekeeping Zone #6 Unit 2 RB Walkdown

Miscellaneous Technical Requirement Manual, 3.14.2, Fire Hose Stations, Circulating Water Pump Structure, Revision 6

Section 1R06: Flood Protection Measures Drawings M-541, Plumbing and Drainage Circulating Water Pump Structure Plan and Details, Revision 6 Miscellaneous Internal Plant Examination, Volume 1, Section 3.3.8 - Internal Flooding Analysis

PB -
PRA -012,
PBAPS [[]]

PRA Internal Flood Evaluation Summary Notebook, Revision 1

P-T-09, Internal Hazards Design Basis Document, Revision 9

Section 1R11: Licensed Operator Requalification Program Procedures

OT -100, Reactor Low Level, Revision 12
OT -111, Reactor Low Pressure - Procedure T-101 Sheet 1,

RPV Control T-102 Sheet 1-3, Primary Containment Control

T-103 Sheet 1, Secondary Containment Control

T-104 Sheet 1, Radioactivity Release

T-111, Sheet 1, Level Restoration

T-116, Sheet 1-2,

RPV Flooding T-204-2/3, Initiation of Containment Sprays Using

RHR T-216-2/3, Control Rod Insertion by Manual Scram or Individual Scram

T-220-2/3, Driving Control Rods during Failure to Scram

T-250-2/3,

RPV Pressure Control using
HPCI with Suction from CST
TQ -

AA-150, Operator Training Programs, Revision 5

Attachment Miscellaneous

PS [[]]

EG0325R, T-100 Scram, Scenario 4, Revision 9

Section 1R12: Maintenance Effectiveness Condition Reports 1165407,

RPS Test Box did not Light During

SI2N-60A-APRM-41C2

1166983, Refurb

APRM Voter Unit Found Defective Upon Installation 1220525, Failure of Unit 3
APRM #1 2/4 Voter 1225141, Replace A19 and A20 Cards in
AP [[]]

RM 2/4 Voter

286163,

APRM -

LM-3-PB3 2/4 Logic Module did not Drop Out RPS Logic

286435, A2 Channel 1/2 Scram During

AP [[]]

RM 3 Logic Module Repair

287120,

APRM Voter Card Failures - Need Accelerated Replacement 1321901,
APRM -LM-3-PB3 Failed
PMT Under C0240771 1322276, Unexpected
RBM Alarm During
AP [[]]

RM #3 Module Swap

1434493, 2/4 Voter Failed to Actuate Trip During Surveillance

  • 1443078, Gaps in the
PCM Process

MA-AA-716-210

  • 1445266, IRs With No/Inaccurate Affected Systems Identified

1451965,

APRM [[]]
HFA Relay Load Currents Required 1452962,
APRM [[]]
HFA Relay Load Currents Required 1452963,
APRM [[]]

HFA Relay Load Currents Required

1452964,

APRM [[]]

HFA Relay Load Currents Required

Miscellaneous

MR Scoping Document, System 60A -
APRM and
LPRM Instrumentation Section 1R13: Maintenance Risk Assessments and Emergent Work Control Procedures
OP -PB-108-101-1002, Control of Protected Equipment Tracking Sheets, Revision
7 ST -O-052-122-2, E-2 Diesel Generator

RHR Pump Reject Test, Revision 9, Performed November 5, 2012 (Yellow Risk) Section 1R15: Operability Evaluations

Procedures SE-16 Bases, Grid Emergency, Revision 12

SE-16, Grid Emergency, Revision 11

Condition Reports 1418236,

WRNM C Reading Higher Than Expected 1418238,

WRNM F Reads Higher Than Expected

1419377, Risk Assessment Required for

WR [[]]

NM's Prior to Refueling

21363, Revision to P2R19 Reload

CCT [[]]
AS 22250,
WR [[]]

NM Identified with a Potential Loose Adapter

23132, NT-2-07-041D Discriminator Curves Not as Expected Miscellaneous Unified Control Room Log, Monday, October 8, 2012, Night Shift

Unified Control Room Log, Tuesday, October 30, 2012, Night Shift

Licensed Operator Training,

PLOT 5060C,

WRNM Instrumentation

Attachment Outage Control Center Log, Tuesday, October 2, 2012, Days Outage Control Center Log, Friday, October 5, 2012, Night Outage Control Center Log, Monday, October 8, 2012, Night

TS 3.3.1.2,
WRNM Instrumentation
TS Bases 3.3.1.2,
WRNM Instrumentation
TS 3.8.1
AC Sources - Operating
TS 3.8.4
DC Sources - Operating
ECR [[]]
PB 94-04697,
RX Recirc Motor A Air
CLR [[]]
DRN Pan
LVL Section 1R19: Post-Maintenance Testing Procedures
ST -M-016-220-2, Main Steam Relief Valve Actuator Functional Test, Revision 6, Performed 09/27/12
SI 2K-54-E22-XXC2, Calibration Check of E22 4kV Bus Undervoltage and Sequential Loading Relays, Revision 5, Performed 09/29/12
SI 2K-54-E42-
XXC 2, Calibration Check of E42 4kV Bus Undervoltage and Sequential Loading Relays, Revision 5, Performed 10/03/12
ST -M-01A-471-2,
MSIV Timing, Springs Only Closure and Position Switch Adjustment, Revision 12, Performed 10/05/12
ST -O-07G-470-2,
MSIV Valve Closure Timing, Revision 17, Performed 10/05/12 ST-O-37C-360-2, Motor Driven Fire Pump Operability Test, Revision 14
ST -O-054-752-2, E-22 4Kv Bus Undervoltage Relays and
LOCA [[]]
LOOP Functional Test and E-22 and E-224 Alternative Shutdown Control Functional Test, Revision 22
SI 2N-60A-APRM-31FS, Functional Check of
APRM 3, Revision 5, Performed 11/30/12 Condition Reports 1422717, Stroke Adjustments Made to

MSIVs

23056, Evaluate

MS [[]]

RV Pressure Switches

1419952, Relay 144-16 Sticking During

SI 2K-54-E22-
XXC 2 1414208,
SI 2K-54-E12-
XXC 2 Relay 144-15 Out of Cal High, Black Box Unsat 1427364, 2B Core Spray Pump Did Not Start In Accordance with E22 Bus
LO [[]]

CA Test

22133, P2R19

MS [[]]

IV-80A As-Found Stroke Time Fast

22697,

MS [[]]

IV Stroke Times Near End of Acceptable Range

1445911,

APRM -

LM-3-PB2 Keylock Switch

1446620, Scheduled Work Not Completed

WO s /

ARs A/R A1638519

Miscellaneous Outage Control Center Log, Thursday, October 4, 2012, Night Technical Requirement Manual, 3.14.1, Water Fire Protection System, Revision 9

TC 12-0192, Exercise the Logic Module Keylock Switch during
SI 2N-60A-APRM-31FS
WC -
AA -111, Attachment 3, Test Results Evaluation Form for
SI 2N-60A-

APRM-31FS, Performed 11/30/12, Revision 4 Section 1R20: Refueling and Other Outage Activities Procedures AO 27.1-2, Unit 2 Reactor Cavity Let Down During Vessel Re-assembly, Revision 13

GP-2, Normal Plant Startup, Revision 130

Attachment

GP -6, Refueling Operations, Revision 22 Operability Evaluation 11-03, Conducted Under
IR 1254155-09
OP -
AA -108-108, Engineering Department Start-up Checklist, Revision
12 OP -
AA -108-108, Unit 2 Startup
PO [[]]
RC Meeting, Revision 12, Performed on 10/15/12
OP -
AA -108-115, Operability Evaluation 12-006 Revision 1,
MO -2-10-025B (
RHR Loop B Inboard Discharge Valve), Revision
11 ST -O-080-675-2, Reactor Pressure Vessel (
ASME Class I) Leakage Pressure Test, Revision
22 ST -R-003-495-2,

CRD Scram Insertion Timing of Selected Control Rods During Hydro, Revision 5

Condition Reports Common Cause Analysis 1434403, Clearance and Tagging Adverse Trend 1422610, Peach Bottom RCR Inadvertent Release of Lube Oil from Turbine Bearing Lift System

  • 1425906, HV-2-16-23169L Leaking By

28185, The

PB 2C20 Startup Critical Occurred Beyond the

ECP

28377, PB 2 Cycle 20 Startup Shutdown Margin Actual Versus Design

1430817, Minor Revision to ST-R-002-900-2(3) Required Miscellaneous Shutdown Safety Approval / Notification Form: Use of 3.0.4.b, Dated 10/12/12

Technical Specification 3.5.2:

EC [[]]

CS - Shutdown, Amendment No. 259

Technical Specification 3.5.2 Bases:

ECCS - Shutdown, Revision 0 General Electric

BWR/4 STS 3.5.2 Bases, Revision 4.0 Unified Control Room Log, Friday, October 12, 2012, Night Shift

Section 1R22: Surveillance Testing

Procedures

ST -M-57B-744-2, Unit 2D 125/250
VDC Battery Service Test, Revision 10, Performed on 10/1/12
SO 40D.7.B, Place Control Room Ventilation Emergency Ventilation in Service from the Control Room, Revision 12
ST -O-054-754-2, E42 4kV Bus Undervoltage Relays and
LOCA /
LOOP Functional Test and E42 and E424 Alternate Shutdown Control Functional Test, Revision 19, Performed 10/04/12 (LOOP only portions)
TC 12-0148, Temporary Change to
ST -O-054-754-2, Revision 19, Performed 10/05/12
ST -O-054-754-2, E42 4kV Bus Undervoltage Relays and
LOCA /LOOP Functional Test and E42 and E424 Alternate Shutdown Control Functional Test, Revision 19, Performed 10/16/12 (LOOP
LOCA portion)
ST -O-080-675-2, Reactor Pressure Vessel (ASME Class I) Leakage Pressure Test, Revision 22, Performed 10/15/12
ST -R-003-495-2,
CRD Scram Insertion Timing of Selected Control Rods During Hydro, Revision
5 ST -R-003-495-2,
CRD Scram Insertion Timing of Selected Control Rods During Hydro, Revision 5, Performed 10/14/12
ST -O-023-301-2,
HPCI Pump, Valve, Flow and Unit Cooler Functional and
IST , Revision 61, Performed on 10/19/12,
ST -O-013-301-2,
RCIC Pump, Valve, Flow and Unit Cooler Functional and

IST, Revision 40

Attachment

ST -O-023-200-3,
HPCI Flow Rate at Less than or Equal to 175 psig, Revision
16 ST -O-013-200-2,
RCIC Flow Rate at Less than or Equal to 175 psig, Revision
16 RT -O-023-725-3,
HPCI Response Time Test, Revision
17 RT -O-013-725-3m

RCIC Response Time Test, Revision 10

ST-O-020-560-2(3), Reactor Coolant Leakage Test, various tests from October 1 through December 31, 2012

Condition Reports 1422221,

ST -O-054-754-2 Failed Acceptance Criteria 1422294, 0

AV030 Failed to Auto Start

22551, Conditional

TC to

SO 40D.1.A

22527, Alarm "Control Room Supply Fan 0A-BV30 Standby Fan" Not Received 1423138,

MCR Vent Rad Monitor Loss of Indication 1427772,
NOS [[]]
ID [[:]]
EDG [[]]
TS Surveillance Requirement Not Met 1427846,
NOS [[]]
ID Shift

SRO Review Failed to Identify Inoperability

1439848, A Change of

TS [[]]

SR 3.8.1.18 Needs to be Made

26616,

NOS [[]]

ID: Enhance Pressure Test IPA Brief for Parallel Activity

26672, Unit 2 Reactor Head Vent

AO -17 No Closed Indication in
MCR 26761, 2R19 Hydro - Leakage Identified on
CRD -2-03-2239 1426762, 2R19 Hydro - Leakage Identified on

CRD-2-03-4259 1426763, 2R19 Hydro - Leakage Identified on CRD-2-03-1823

26764, 2R19 Hydro - Leakage Identified on CRD-2-03-5011

26765, 2R19 Hydro - Leakage Identified on CRD-2-03-4235

26785, 2R19 Hydro - Leakage Identified on

XFC -2-02-73H 1426794, 2R19 Hydro - Packing Leak on

HV-2-06-35A 1426795, 2R19 Hydro - Packing Leak on HV-2-06-34B

26796, 2R19 Hydro - Leak From HV-2-01A-84C Test Tap Cap

26798, 2R19 Hydro - Test Tap Cap Leak on HV-2-13C-47A

26800, 2R19 Hydro - Leakage Identified on

RV -2-12-8474 1426802, 2R19 Hydro - Leakage Identified on

HV-2-12-17 1426803, 2R19 Hydro - Packing Leak Identified on RTV-2-12A-20530A

26807, 2R19 Hydro - Leakage Identified at Dragon Block Valve

26823, 2R19 Hydro - Packing Leak on AO-2-01A-080D

26824, 2R19 Hydro - Packing Leak on HV-2-10-88

26825, 2R19 Hydro - Packing Leak on

MO -2-06-029A 1429185, Recommend Tuning of Unit 2

HPCI Governor Controls 1438936, Step Increase in Unit 2 Drywell Unidentified Leak Rate Identified

Miscellaneous Event Notification 48376, Both Trains of Control Room Emergency Ventilation Out-of-Service

PBAPS [[]]
OE 301444, Failure of Control Room Emergency Ventilation Fan to Auto Start
PBAPS [[]]
OE 301456, Delayed Re-energizing of 4kV Emergency
AC Bus During Loss of Power
ST due to Failed Relay
PBAPS Unit 2
TS Bases 3.0.6
UFSAR Table 8.5.1, Sequence of Events in the Automatic Application of Emergency
AC Loads on
LOCA without Offsite Power, Revision 21
UFSAR Table 8.5.4, Sequence of Events in the Automatic Application of Emergency
AC Loads on
LOCA with One Offsite Source Available, Revision
21 UFSAR Table 8.5.5, Sequence of Events in the Automatic Application of Emergency
AC Loads on
LO [[]]

CA with Two Offsite Sources Available, Revision 21 Outage Control Center Log, Thursday, October 4, 2012, Night

Attachment Unified Control Room Log, Thursday, October 4, 2012, Day Shift Unified Control Room Log, Thursday, October 4, 2012, Night Shift Unified Control Room Log, Friday, October 5, 2012, Day Shift Unified Control Room Log, Monday, October 15, 2012, Night Shift

Outage Control Center Log, Monday, October 15, 2012, Night

Section

1EP 6: Drill Evaluation
EP -AA-112-200, "TSC Activation and Operation," Revision
8 EP -
AA -122-1001-F-10, "Drill & Exercise Post-Event Critique & Report Development Guidance," Revision C
EP -

AA-122-1001-F-11, "Drill & Exercise Comment & Feedback Form," Revision D Exelon Nuclear Emergency Preparedness Peach Bottom - December 12, 2012 Station Drill

Controller\Evaluator Instructions

Peach Bottom Station December 12, 2012, Station DEP Drill

Peach Bottom - Scenario 0839, Revision 3

Peach Bottom December 12, 2012, Medical Drill Revision A

SE -12, Injury Response, Revision 23 Section 2
RS 05: Radiation Monitoring Instrumentation Calibration & Test Procedures:
SI 2R-63F-050-A1
CE , Revision 11, Main Stack Rad Monitor RY-0-17-050A Electronics Calibration Check
SI 2R-63F-050-A1
FQ , Revision 12, Main Stack Rad Monitor RY-0-17-050A Functional Check
SI 2R-63F-050-B1
CE , Revision 13, Main Stack Rad Monitor
RY -0-17-050B Electronic Calibration Check
SI 2R-63F-050-B1FQ, Revision 13, Main Stack Rad Monitor RY-0-17-050B Functional Check
SI 2F-40B-2805-A1

CE, Revision 2, Calibration Check of RB Vent Stack Flow Loop

Instruments

FT 2805A and
FR 2805
SI 2F-40B-2805-B1
CE , Revision 2, Calibration Check of
RB Vent Stack Flow Loop Instruments
FT 2805B and
FR 2805

SI2R-63E-2979-A1CE, Revision 10, Vent Stack Rad Monitor RY-2979A Electronic Calibration

Check

SI 2R-63E-2979-A1

FQ, Revision 9, Vent Stack Rad Monitor RY-2979A Electronic Functional

Check

SI 2R-63E-2979-B1
CE , Revision 10, Vent Stack Rad Monitor
RY -2979B Electronic Calibration Check
SI 2R-63E-2979-B1FQ, Revision 11, Vent Stack Rad Monitor RY-2979B Electronic Functional Check
SI -3F-40B-3805-A1

CE, Revision 6, Calibration Check of RB Vent Stack Flow Loop

Instruments

FT 3805A and
FR [[]]
3805 SI 3F-40B-3805-B1
CE , Revision 5, Calibration Check of
RB Vent Stack Flow Loop Instruments
FT 3805B and FR 3805
SI 3R-63E-3979-A1

CE, Revision 10, Vent Stack Rad Monitor RY-3979A Electronic Calibration

Check

SI 3R-63E-3979-A1
FQ , Revision 8, Vent Stack Rad Monitor
RY -3979A Electronic Functional Check
SI 3R-63E-3979-B1CE, Revision 11, Vent Stack Rad Monitor RY-3979B Electronic Calibration Check
SI 3R-63E-3979-B1

FQ, Revision 10, Vent Stack Rad Monitor RY-3979B Electronic Functional Check

Attachment

SI 2R-63M-350-
XXC 1, Revision 8, Electronic Calibration/Functional Check of the Radwaste Effluent Radiation Monitor
RIS 0-17-350

ST-0-63M-810-2, Revision 6, Liquid Radwaste Monitor and Discharge Valve Functional Test Section 2RS06 Annual Radiological Effluent Release Report, January 1, 2011 through December 31, 2011,

dated 4/27/12

OD [[]]

CM, Revision 14 Liquid Radwaste Discharges: 605-12, dated 8/15/12; 516-12, dated 7/16/12; 517-12, dated

7/16/12; 716-12, dated 9/18/12; 708-12, dated 9/18/12

Weekly Gaseous Iodine and Particulate dated: 4/4/12; 2/8/12; 8/22/12; 7/23/12; 5/30/12

Condition Reports: 01445222; 01440410; 01439489; 01299543; 01328430 Check-In Self-Assessment: 1201437-02,

KT 7R, Met Tower,

REMP/RETS

1141803-01, Radiochemistry Instrumentation

1133689-02, Chemistry Laboratory and Radiochemistry Quality Control

1165276-02, Pre-NRC Self-Assessment for Procedure 71124.06

21090-02,

RECP and

ODCM Pre-NRC Assessment Eckert & Ziegler Analytics Cross-Check Program results for: 1st Quarter 2012; 2nd Quarter 2012; 3rd Quarter 2012

Procedure

CY -
AA -130-201, Revision 2, Radiochemistry Quality Control Inspection & Test Procedures:
RT -I-037-239-2, Revision 6, Recombiner Filter A Heat Detectors Functional Test

RT-I-037-240-2, Revision 7, Recombiner Filter B Heat Detectors Functional Test RT-M-37B-359-2, Revision 0, Recombiner Building Exhaust Filter Train A Deluge System

Airflow Test

RT-M-37B-360-2, Revision 0, Recombiner Building Exhaust Filter Train B Deluge System

Airflow Test

ST -M-09A-600-2, Revision 14,
SBGT System Filter Train A
ST -M-09A-601-2, Revision 14,
SBGT System Filter Train B
ST -M-037-351-2, Revision 3,
SBGT Filter Train A Deluge System Nozzle and Piping Inspection
ST -M-037-352-2, Revision 4,
SBGT Filter Train B Deluge System Nozzle and Piping Inspection
ST -M-037-353-2, Revision 1,
SBGT Filter Train A Deluge System Airflow Test
ST -M-037-354-2, Revision 1,
SBGT Filter Train B Deluge System Airflow Test
ST -M-40D-905-2, Revision 19, Control Room Emergency Ventilation Filter Train A Test

ST-M-40D-910-2, Revision 20, Control Room Emergency Ventilation Filter Train B Test

Section

4OA 1: Performance Indicator Verification
MSPI Deviation Reports and System Manager Notebooks: October 2011 through September 2012, Unit 2 and Unit 3

RHR/HPSW

October 2011 through September 2012, Unit 2 and Unit 3 ESW

October 2011 through September 2012, Unit 2 and Unit 3 EDGs

October 2011 through September 2012, Unit 2 and Unit

3 HP [[]]
CI October 2011 through September 2012, Unit 2 and Unit
3 RCIC Procedures:
ER -AA-600-1047, Mitigating Performance Index Basis Document, Revision 7
ER -
AA -2008,
MS [[]]
PI Failure Determination Evaluation, Revision 2
ER -
AA -2020,
IN [[]]

PO Consolidated Events System, Revision 7

Attachment

LS -
AA -2001, Collecting and Reporting of
NRC [[]]
PI Data, Revision
14 LS -
AA -2080, Monthly Data Elements for
NRC [[]]
SSFF s, Revision
4 LS -
AA -2200,
MS [[]]

PI Data Acquisition and Reporting, Revision 5

Miscellaneous:

NEI 99-02, Regulatory Assessment Indicator Guideline, Revision 6
PBAPS [[]]

MSPI Basis Document, Revision 7

Section

4OA 2: Identification and Resolution of Problems Procedures

LS-AA-125, CAP Procedure, Revision 17

Condition Reports *1429435, Nut Found in E3 EDG Room

  • 1438812, Documentation of
SOC Member Review of

SY Procedure

1442958, Analysis of Drywell Head Strongback Incorrectly Used

CMT [[]]

RS

1445119, Insulation Not Able to be Reused (Due to 2 'B' RHR Flow orifice flange leak)

  • 1451404, Packing Leak on AO-2-23-053 1419073, Nuclear Oversight Identified: Operations Shortfalls in Use of Human Performance 1423654, Adverse Trend in Clearance and Tagging Events

1430391, Declining Trend in Site Configuration Control

1430644, Corporate Escalation due to Continued Adverse Human Performance Event Trend

25757, Nuclear Oversight Identified: Lapses in Work Standards Results in Adverse Trend 1430748, Elevation for Maintenance Department Human Performance at Peach Bottom 1394685, Adverse Trend in Maintenance Department and Crew Clock Resets

Miscellaneous Peach Bottom Station Trend Review - 2Q12 Analysis Peach Bottom Station Trend Review - 3Q12 Analysis Section

4OA 3: Follow-up of Events and Notices of Enforcement Discretion Procedures
OP -PB-108-111-1001, Preparation for Severe Weather, Revision 8
OP -
AA -108-111-1001, Severe Weather and Natural Disaster Guidelines, Revision 9
SY -

AA-101-146, Severe Weather Preparation and Response, Revision 0

Condition Reports 1432999, Loss of 28 of 97 EPZ Sirens ( 25% Threshold) *1434345, Wind Speed Instrument Use

1431972, Mechanically Restrain Cooling Tower Fans In Accordance with

OP -

PB-108-111-1001

1451414,

RT -M-045-990-2 Could Not Be Performed for D03 (sand bags outside E3
EDG Maintenance door) 1418320,
MSRV /

MSSV Failed P2R19 As-Found Lift Tolerance

Miscellaneous

SE -4 Bases, Flood - Bases, Revision 22
SE -4 Procedure, Flood - Procedure, Revision 32

AO 28.2, Response to High/Low River Level, Revision 2 SE-3 Procedure, Loss of Conowingo Pond - Procedure, Revision 21

eSoms, Peach Bottom Unified Control Room Log on October 30

Attachment Hurricane Sandy Plant Status Matrix on October 30 Technical Specification

SRV Surveillance Requirements
SR 3.4.3.1 Apparent Cause Evaluation 1120516-04, Historical
SRV As-Found Lift Setpoint Drift
NRC [[]]
PI&R Inspection Report 05000277/2011010
AND 05000278/2011010
PBAPS Maintenance Rule Scope and Performance Monitoring, System 01A-Main Steam: Main Steam Safety Valves and Main Steam Relief Valves
PORC Meeting,
ACE - Multiple
MSRV /MSSV Failed P2R19 As-Found Lift Tolerance 12/11/12 Section
4OA 5: Other Activities Procedures
ER -AA-5400, Revision 5, Buried Piping and Raw Water Corrosion Program (BPRWCP)
ER -
AA -5400-1001, Revision 5, Raw Water Corrosion Program Guide
ER -
AA -5400-1002, Revision 4, Buried Piping Examination Guide
ER -
AA -5400-1003, Revision 4,
BPRWCP [[]]
PI s
LS -
AA -126-1005, Revision 5, Self Assessment
NRC Buried Piping
TI Inspection (Phase1)
CSI Report 0600.109-02, Revision 0,
PBAPS Buried Piping (Units 1, 2 & 3) Program Risk Ranking 11/16/2009
NES -
MS 015.2, Reasonable Assurance Guideline
PBAPS Buried Pipe and Raw Water System Long Term Asset Management Strategy (Revision 5, February/2012)
MPR -3670 Revision 0, Buried Piping Alternatives Analysis PB-11-0355 (149784) 4" Radwaste Discharge Mitigation Project
PB -12-0111

PBAPS Buried Service Water Mitigation Project

Prioritization of Underground Piping and Tanks

NEI 09-14, Revision 1, System and Component Tables (6/28/2012)
EN -AA-408-4000, Revision 3, Radiological Groundwater Protection Program Implementation
EN -
AA -407, Revision 5, Response to Inadvertent release of Licensed Materials to Groundwater, Surface Water or Soil
RP -
AA -228, Revision 1,
10 CFR 50.75(g) and 10

CFR 72.30(d) Documentation Requirements

Miscellaneous

NRC Temporary Instruction 2515/182, 11/17/11; Review of the Implementation of the Industry Initiative to Control Degradation of Underground Piping and Tanks
NEI 09-14 (Revision 1), December 2010; Guideline for the Management of Underground Piping and Tank Integrity
NEI 09-14 (Revision 2) March 2011, Industry Approach for Development of Inspection Plans that Establish Reasonable Assurance of Structural and Leakage Integrity of Buried Piping

TI-187 Procedures SE-4, Flood Procedure, Revisions 31 and 32

SE-4 Bases, Revision 22 Condition Reports *1406251, Fukushima - Flex Conduit Fitting Separated

  • 1414866, Fukushima - Flood W/Ds - Valves Not Stroked Periodically

1444588, Fukushima - Available Physical Margin (APM) at Peach Bottom 1373999, Inspection Deficiencies on Sluice Gate 3A 1404681,

EACE Rejected at

MRC

1403209, Documentation of Water Intrusion Open Deficiencies

Attachment 1405635, A1821132 Should be Pulled Into 2R19 1416066, Fukushima Flood W/Ds -

AR to Inspect E224-P-A Conduits 1416069, Fukushima Flood W/Ds -
AR to Inspect E124-P-A Conduits 1420399, E224-P-A
MCC in Need of

PM

20405, Opportunity to Seal Conduits in E224-P-A When De-energized

1451882, Contingent Work Order for Conduit Flood Seals in

MCC E224

PA

1388780, Water Intrusion in 2C RHR Room

1398861, 3C

RHR [[]]
HPSW Return Pipe Penetration Seal Degraded 1393061, Fukushima External Flooding Protection Feature Walkdown
ECT 1401537, Fukushima External Flood - Diesel Generator

CRLS

1402625, Fukushima Flooding Feature Walkdowns - DG Inaccessible Seals

1392977, Diesel Building Dirty Oil Storage Tank Trouble Alarm

1387260, Received Alarm Diesel Building Dirty Oil Storage Tank Trouble 1408393, Diesel Building Dirty Oil Storage Tank Trouble Alarm 1410422, Received Alarm "Diesel Building Dirty Oil Storage Tank"

1411311, SE-4 Revision

1411382, Fukushima:

CRC Consider

SE-4 for EO Continuing Training

1454435 1454054 1454016 1441277 1428739 1431993 1414866 1414866 1409236 1406272 1410116 1401975 1401971 1397807 1396442 1396021

Drawings M-541, Plumbing and Drainage Circulating Water Pump Structure Plan and Details, Revision 6 Miscellaneous

NEI 12-07, Guidelines for Performing Verification Walkdowns of Plant Flood Protection Features, Revision 0-A
PBAPS [[]]
IPEEE , May 1996 P-T-07, External Hazards Design Basis Document, Revision 2 Summary Results for External Flooding Simulations at
PBAPS [[]]
UFS [[]]
AR Section 2.4.3.5 - Flood
UFS [[]]
AR Section 12.2.5 - Diesel Generator Building
U.S. [[]]
NRC Letter dated November 22, 1999:
SER of
PBAPS [[]]
IPE [[]]

EE

TI-188 Condition Reports 1459805 1459810 1459813 1459830 1438055 1437865

1437853 1411581 1428651 1428745 1429745 1419993 1426027 1425997 1425994 1425673 1424737 1424719 1424692 1424662 1423731 1416151 1413655 1413652

1413285 1411581

Miscellaneous

EPRI Report 1025286, Seismic Walkdown Guidance, June 2012
PBAPS [[]]
IPE [[]]
EE , May 1996 P-T-07, External Hazards Design Basis Document, Revision 2
U.S. [[]]
NRC Letter dated November 22, 1999:
SER of
PBAPS [[]]
IPE [[]]

EE

Attachment Section 4OA7: Licensee-Identified Violations

Procedures

EP -

AA-1007, Revision 23 and 25

Condition Reports 1439489,

ODCM Change Did Not Include

EAL Recalculation

1440410,

ODCM X/Q Values to be Updated in
ODCM Revision Planned 1418320, P2R19
MSRV /

MSSV As-Found Lift Test Results 1421109, P2R19 - SRV S/N 17 and S/N 81 Failed Manual Lift

1445263, 2R19

SRV /

SV A/F Test Results - Perform (a)(1) Determination

1411036, Unit 2 CV #4 Upper Push Rod Pin

1411069,

PS -4121A Found Out of Cal Low During
SI 2P-5-4121-A1C2 1411469,
CV -2 Unit 2 Investigate for Possible Pin Migration 1411485,

CV-3 Unit 2 Upper Control Arm Clevis Not Assembled as per GE

1411488, Possible Grub Screw Migration on Upper Control Arm Clevis

1415734, U2 CV 1 Lower Spring Housing Lower Guide

1416600,

SMT -

CV 4 Upper Control Arm / Lower Tension Rods

1416922,

SMT -
CV 4 Actuator Push Rod 1429163,
EOC Inspection
FAS for
TCV 2 1423668, Replacement of Barksdale Switch for

CAP Investigation

1450780, Perform Mid-Cycle

PS -4121C and 4121D
WO s /
AR s A1878916, Failure Analysis of the
RETS [[]]

TCV RPS Pressure Switches

Miscellaneous

NEI 99-01, Methodology for Development of Emergency Action Levels, Revision 5
PBAPS White Paper: Evaluation of the Effects on
EAL Classification with Peach Bottom Vent Stack
EAL Thresholds Values Higher than Appropriate
UFSAR Section 7.12.5.5.2, Revision 21
U.S [[]]
NRC Inspection Report 2011-010, PI&R Biennial Team Inspection
PBAPS Unit 2

TS Bases 3.4.3, Safety Relief Valves and Safety Valves

Technical Specification

SRV Surveillance Requirements

SR 3.4.3.1

Attachment

LIST [[]]
OF [[]]
ACRONY [[]]
MS [[]]
ADA [[]]
MS Agency wide Documents Access and Management System
ALA [[]]
RA as low as is reasonably achievable
AP [[]]

RM average power range monitor

AR action request
ARC alarm response card

CAP corrective action program CFR Code of Federal Regulations

CRs condition reports

DBD design basis document
DC direct current

ECT emergency cooling tower EDG emergency diesel generator

ESW emergency service water
FS [[]]

AR final safety analysis report

GPI groundwater protection initiative
HEPA high efficiency particulate air
HPCI high pressure coolant injection
HP [[]]

SW high pressure service water

HX heat exchanger

IMC inspection manual chapter
INPO Institute of Nuclear Power Operations

IP inspection procedure IR issue report

LCO limiting condition for operation

LDE lens dose equivalent
LER s licensee event reports
MCR main control room
MCR [[]]

EV main control room emergency ventilation

MDA minimum detectable activity

MOV motor operated valve

MR Maintenance Rule
MSPI mitigating system performance index

MSIV main steam isolation valve NCV non-cited violation

NEI Nuclear Energy Institute
NI [[]]
ST National Institute of Standards and Technology
NRC Nuclear Regulatory Commission

NVLAP National Voluntary Laboratory Accreditation Program OCC outage control center

OD operability determination
OD [[]]

CM offsite dose calculation manual

OOS out-of-service
OSLD optically stimulated light dosimeter
PARS publicly available records
PBA [[]]

PS Peach Bottom Atomic Power Station

PI performance indicator

PI&R problem identification and resolution

PMT post-maintenance test

Attachment

RAI request for additional information
RB reactor building
RE [[]]

TS radiological effluents technical specification

RFO refueling outage

RG regulatory guide

RHR residual heat removal
RPS reactor protection system

RPT recirculation pump trip RRP reactor recirculation pump

RTP rated thermal power
RW [[]]
CU reactor water cleanup
SDE shallow dose equivalent

SFP spent fuel pool SRV safety relief valve

SSCs structures, systems, and components

STs surveillance tests

SV safety valve
SWEL seismic walkdown equipment list
TCV turbine control valve
TE [[]]

DE total effective dose equivalent

TI temporary instruction

TS technical specification
UFSAR updated final safety analysis report
WO s work orders
WR [[]]
NM wide range neutron monitoring