05000361/LER-1982-103, Followup LER 82-103/03X-2:on 820825,sample Isolation Valve 2HV-0517 Hot Leg Breaker 2BJ-23 Tripped on Overload While Attempting to Close Valve.Caused by burned-out Motor on Operator.Motor Replaced.Procedures Revised

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Followup LER 82-103/03X-2:on 820825,sample Isolation Valve 2HV-0517 Hot Leg Breaker 2BJ-23 Tripped on Overload While Attempting to Close Valve.Caused by burned-out Motor on Operator.Motor Replaced.Procedures Revised
ML20072V048
Person / Time
Site: San Onofre Southern California Edison icon.png
Issue date: 03/30/1983
From: Ray H
SOUTHERN CALIFORNIA EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
Shared Package
ML20072U993 List:
References
LER-82-103-03X, LER-82-103-3X, NUDOCS 8304110493
Download: ML20072V048 (3)


LER-2082-103, Followup LER 82-103/03X-2:on 820825,sample Isolation Valve 2HV-0517 Hot Leg Breaker 2BJ-23 Tripped on Overload While Attempting to Close Valve.Caused by burned-out Motor on Operator.Motor Replaced.Procedures Revised
Event date:
Report date:
3612082103R00 - NRC Website

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ATTACHMENT TO LER 82-094 SOUTHERN CALIFORNIA EDISON COMPANY SAN ONOFRE NUCLEAR GENERATING STATION UNIT No. 2, DOCKET No. 50-361 SUPPLEMENTAL INFORMATION FOR CORRECTIVE ACTIONS However, due to the difficulty of obtaining the necessary vendor data, all procedure revisions are not expected to be completed until December 31, 1983.

ATTACHMENT TO LER 82-103 SOUTHERN CALIFORNIA EDISON COMPANY SAN ONOFRE NUCLEAR GENERATING STATION UNIT No. 2, DOCKET No. 50-361 SUPPLEMENTAL INFORMATION FOR CORRECTIVE ACTIONS However, due to the difficulty of obtaining the necessary vendor data, all procedure revisions are not expected to be completed until December 31, 1983, i

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