05000361/LER-2008-001, Regarding Valid Actuation of Emergency Feedwater System Following Main Feedwater Pump Trip

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Regarding Valid Actuation of Emergency Feedwater System Following Main Feedwater Pump Trip
ML080570093
Person / Time
Site: San Onofre Southern California Edison icon.png
Issue date: 02/22/2008
From: Ridenoure R
Southern California Edison Co
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
LER 08-001-00
Download: ML080570093 (2)


LER-2008-001, Regarding Valid Actuation of Emergency Feedwater System Following Main Feedwater Pump Trip
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(iv)(A), System Actuation
3612008001R00 - NRC Website

text

JSOUTHERN CALIFORNIA EDISON An EDISON INTERNATIONAL Company Ross T. Ridenoure VP and Site Manager San Onofre Nuclear Generating Station February 22, 2008 U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555-0001

Subject:

Docket No. 50-361 Licensee Event Report No. 2008-001 San Onofre Nuclear Generating Station, Unit 2

Dear Sir or Madam:

In compliance with 1 OCFR50.73(a)(2)(iv)(A), this submittal provides Licensee Event Report (LER) 2008-001 to report an event that resulted in valid actuation of the emergency feedwater system. Neither the health nor the safety of plant personnel or the public was affected by this occurrence.

If you require any additional information, please contact me.

Sincerely, Unit 2 LER No. 2008-001 cc:

E. E. Collins, NRC Regional Administrator, Region IV C. C. Osterholtz, NRC Senior Resident Inspector, San Onofre Units 2 & 3 Mail Drop D45 P.O. Box 128 San Clemente, CA 92672 949-368-6255 PAX 86255 Fax: 949-368-6183 Ross.Ridenoure@sce.com

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Abstract

On 1/23/08, at about 1415 PST, with SONGS Unit 2 in Mode 1 at about 95 percent power, one of two main feedwater (MFW) [SJ] pumps tripped on low oil pressure. Control room operators manually actuated the emergency feedwater system (AFW) [BA] in accordance with plant procedures. The AFW system responded successfully. Control room operators reduced reactor power level to about 65 percent which can be sustained with one normal feedwater pump in operation.

The AFW manual actuation by plant operators was in response to the MFW pump trip. The MFW pump trip was due to overadjustment of the pump lubricating oil pressure regulator. Maintenance workers used the pump overhaul procedure that did not provide sufficient detail to adjust the oil pressure regulator while the pump is on-line.

The oil pressure regulator was correctly adjusted and the Unit was returned to power. SCE is completing a cause evaluation which may identify additional corrective actions.

All systems responded as designed and Control Room personnel acted timely and correctly. Neither the health nor the safety of plant personnel or the public were affected by this occurrence.

No valid actuation of the AFW due to inappropriate procedures has occurred over the last 3 years.