05000361/LER-1993-004

From kanterella
Jump to navigation Jump to search
LER 93-004-00:on 930802,portions of Shift Surveillance Not Performed.Caused by Personnel Error.Plant Operators Counseled on procedures.W/930901 Ltr
ML20056H136
Person / Time
Site: San Onofre Southern California Edison icon.png
Issue date: 09/01/1993
From: Krieger R
SOUTHERN CALIFORNIA EDISON CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-93-004-01, LER-93-4-1, NUDOCS 9309080272
Download: ML20056H136 (2)


LER-2093-004,
Event date:
Report date:
3612093004R00 - NRC Website

text

______ . _ _ _ _ ___ __

< . ~

Southem Califomia Edison Company P o Box 128 SAN CL E M E NT E. C ALIF ORNi A 92674-0128 R w M RIE G E R ,E t t Po so.E m.... September 1, 1993 , 3...a.

.x a .. r.. .. .., .o.

U. S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555

Subject:

Docket No. 50-361 30-Day Report Licensee Event Report No.93-004 San Onofre Nuclear Generating Station, Unit 2 l

l Pursuant to 10 CFR 50.73 (d) , this submittal provides the required 30-day written Licensee Event Report (LER) for an occurrence involving an incomplete l Technical Specification Once-A-Shift required surveillance. Neither the health nor the safety of plant personnel or the public was affected by this occurrence. i 1

If you require any additional information, please so advise.

Sincerely, n/l ,'/

f j

. bH %

, /

Enclosure:

LER No.93-004 cc: B. H. Faulkenberry (Rt:gional Administrator, USNRC Region V)

C. W. Caldwell (USNRC Senior Resident Inspector, Units 1, 2 and 3)

M. B. Fields, NRC Project Manager, San Onofre Units 2 & 3 Institute of Nuclear Dower Operations (INPO) 07006:

9309080272 DR 930901 Pa ADOCK 05000361 J '

PDR w: I

-I i

O I

, j LICENSEE EVE 41 REPORT (LER) f acility Name t1) Pape (3) l' Docket Number (2) i i 4 5

SAN ONOFRE NUCLEAR GENERATING STATION. UNIT ? !O!5!O!O!Of3!6!1 1!of!0!1 f Title (Ti INCOMPLETE ONCE-A-SHIFT OPERATIONS SURVEILLANCE j EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTeER FACILITIES INVOLVED (8) l l Month Day m Year Year '/// ' Sequential /// Revision ' Month Day Year facility Namas Docket Number (s) [

. /// Nunber /// Number l j NONE Of5!01O!O! ! ! l O! 8 . 0! 2 9! 3I 9! 3 0t0!4 0t0 0!9 01 1 91 3 O! 5! 0! O! 0! ! !

OPERATikG THIS REPORT 15 SUBM;ITED PURSUANT TO 'HE REQUIREMENTS OF 10CfR MODE (9) 4 ' (Check one or more of the folIowing) (11)

_ 20.402(b) _ 20.405(c) _ 50.73(a)(2)(iv) l_ 73.71(b) i POWER _ 20.405(a)(1)(i) _ 50.36(c)(1) _ 50.73(a)(2)(v) 73.71(c) g_. other  !

LEVEL _ 20.405(a)(1)(li) _ 50.35(c)(2) _ 50.73(a)(2)(vii) w (Specify in  !

(10) t  ! O 20.405(a)(1)(iii) 1 50.73(a)(2)(1) 50.73(a)(2)(viii)(A) Abstract below and t

///////////////////////// __

20.405(a)(1)(tv) 50.73(n)(2)(ii) _ 50.73(a)(2)(viii)(B) in text)

///////////////////////// _

,20.405(a)(1)(v) __ 50.73(n)(2)(iii), __ 50.73(a)(2)(x) ,

/////////////////////////

'///////////////////////// . ,

I

/ LICENSFE CONTACI FOR THIS LER (12)

/ l lName f- f ' y/

/ n '

TElf PHONE NU%ER R. W. Krieger. Vice President

! l ic UMG ,pk ion // ,71114!'3!6!Bf-!6!215!5 AREA CODE 6

COMPLETEONELyL"0REACHCOMPONENyFAILUREDESCRIBEDINTHISREPORT(13) l CAUSE jSYSTEM jCOMP0hENT MANUFAC- REPORTABLE !/////// CAUSE SYSTEM jCOMPONENT MANUFAC- 'REPORIABLE, //////  !

I l TURER TO NPRDS /////// TUF.ER TO NPRDS //////

f I f ! f f f f g/////// 1 1 ! ? 1 ! ! ////// j

!  !  ! ! !  ! ! !  !///////!  !  ! ! !  ! ! ! //////  !

SUPPLEMENTAL REPORT EXPECTED (14) Month Day ' Year  !

Expected Submission

~' F' Date (15)  !

I ! Yes (if ves, complete EXPECTED SUSMISSION DATE) !xx! No  !  !  !  !

! ABSTRACT (Limitto1400 spaces, i.e., approximately fifteen single-space typewritten lines) (16)  !

On August 2, 1993, at approximately 1900, during a review of Technical Specification (TS) shift surveillances, it was determined that some portions of a shiftly surveillance i had not been performed. This shiftly surveillance had been successfully performed on l 4

August 1 at 2105, and on August 2 at 2030, with all systems found OPERABLE. Therefore, I

, all systems were, in fact, OPERABLE during this period and there was no safety I significance to this event.

SCE Operations procedures explicitly require that the entire surveillance procedure is  ;

to be used, and any inapplicable steps marked 'N/A". Contrary to this requirement, the operator failed to verify that the procedure copy used to perf onn the surveillance was complete., resulting in only 2 of 22 items being surveilled. Further, the normal review and approval of this procedure by the Control Operator and Control Room Supervisor failed to identify the incomplete surveillance.

The root cause of this event was cognizant personnel error on the part of: (1) the operator (utility, licensed) who perfonned this surveillance; and, (2) the two supervisors (utility, licensed) who had oversight responsibilities over the operator, and who reviewed and approved the incomplete surveillance.

As corrective action, the three plant operators involved have been counselled regarding the use of procedures. This event is also being reviewed by all plant operators.

A review of previous LER's did not reveal any similar events.

l

.. .