LER-1982-034, Forwards LER 82-034/01T-0.Detailed Event Analysis Submitted |
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Southern California Edison Company I" -s q, g S AN ONOFRE NUCLE AR GENER ATING ST A TRON 88.0. box 128 p'
'k [ h S AN C LEMEN TE, C ALIFORNI A 92672 H. B. R A Y July 2, 1982
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ST ATION M AN AGE A (734)49,-7700 U. S. Nuclear Regulatory Commission Office of Inspection and Enforcement Region V 1450 Maria Lane, Suite 210 Walnut Creek, California 94596-5368 Attention:
Mr. R. H. Engelken, Regional Administrator
Dear Sir:
Subject: Docket No. 50-361 14-day FoiIow-up Report Licensee Event Report No.82-034 San Onofre Nuclear Generating Station Unit 2
Reference:
Letter, H.B. Ray (SCE) to R.H. Engelken (NRC),
Written Confirmation of Reportable Occurrence, dated June 22, 1982 In accordance with Appendix A Technical Specification 6.9.1.12.b to Operating License NPF-10, for San Onofre Nuclear Generating Station Unit 2, this submittal provides the required 14-day follow-up and Licensee Event Report (LER) involving the Core Protection Calculator (CPC).
LER No.82-034 is enclosed.
As stated in the referenced letter, during performance of.the post-core hot f unctional testing, discrepancies were discovered involving Reactor Coolant Pump (RCP) shaft speed and Control Element Assembly (CEA) inputs to the CPC.
Our investigations indicate that these were two separate problems.
RCP Shaft Speed inputs I
1.
Problem Description The RCP shaft speed input problem was originally identified in May during Post Core Hot Functional Instrument Correlation Tests. The CPC operator reported that the CPC point identifications (PID's) for the RCP shaft speed displayed at the CPC operator's console did not correspond to actual pump inputs.
820710241 820702 gDRADOCK 05000361 PDR J $"k
Mr. R. H. Engelken July 2, 1982 2.
Cause of Occurence The problem resulted because the plant RCP numbering scheme did not appear to correspond to the vendor's CPC software numbering. The vendor issued a design change on June 10, 1982 to make revised RCP assignments compatible with his understanding of the field wiring of RCP shaft speed inputs.
This action was incorrect. Subsequent investigation determined that the originally wired RCP shaft speed input was correct. This was verified by disconnecting individual RCP speed inputs to the RCP sensors and verifying the correct CPC operator's consolo indication. The vendor then cancelled the original design change on June 22, 1982, and the wiring was restored and tested.
3.
Corrective Action
No additional corrective actions are required.
4.
Impact on Plant Safety If the suggested RCP wiring change input to the CPC's had been made, the CPC's would have been operating with RCP's juxtaposed in its logic. This would have had no ef fect on safety, for flow related events where all RCP's are equally affected.
For example, an electrical frequency transient would be seen by all RCP's and would thus be seen in the CPC's as affecting all the RCP's, however they were configured. For any RCP coastdown combination, from loss of ore RCP up to and including a complete loss of flow, protection would not have been degraded. The CPC software is configured to provide a trip signai upon detection of loss of any one or more RCP's, irrespective of which RCP is lost.
Under certain conditions, normal steady-state operation may have been seen by the CPC as slightly different from actual plant conditions.
This might occur if one pump is rotating at a different speed because of individual pump / motor characteristics or loop flow resistance characteristics. Had the suggested input Juxtacosition been made, the deviating pump speed would be seen as being in a different loop from the actual deviating loop.
Slightly different total mass flows and delta-T power calculation could have occurred.
This is not considered a problem as no reduction of the protection provided by the CPC would result.
b
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'Mr. R. H. Engelken July 2, 1982 CEA Position Indication inputs 1.
Problem Description i
The CEA position indication problem was identified on June 10, 1982 during Control Element Drive Mechanism (CEDM) Rod Drop Testing. It was noticed that the CPC operator's console CEA assignments did not correspond to actual CEA assignments.
2.
Cause of Occurence-Investigation of the problem revealed that while adequate procedures existed to implement and verify the CEA input order, an error was made in the implementation. The CPC software inputs were assigned according to increasing CEA subgroup number while the hardware j
provided CEA inputs according to increasing CEA number.
l 3.
Corrective Action
The decision was made to revise the CEA inputs to make them compatible with the existing CPC software. The vendor issued a design change on June 23, 1982 to revise the CEA inputs. This design change included rewiring the CEA inputs to the CPC and conducting verification checks of the circuits to verify the correct pin assignments.
l A review of the mechanism for this error has indicated it is an independent event related to the hardware / software interface. The vendor is developing a software / hardware interface specification to clarify the CPC assembly and testing. This will preclude recurrence l
on future installations.
l 4.
Impact on Plant Safety l
l If the CEA assignment problem had remained undetected and the CPC had been in service, response would have been conservative compared to the FSAR analysis. The CEA assignments as seen by the CPC's were sufficiently juxtaposed so that any authorized bank positioning in
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the core (i.e., outside of the top deadband) would have resulted in l
very conservative subgroup or out-of-sequence penalty f actors being j
applied to the DNBR and Local Power Distribution (LPD) calculations.
This would have resulted in a reactor trip or would have alerted the operators to the problem.
If all the CEA's are out of the core, no penalty factors would have been applied.
In particular, during the plant startup procedure the CPC's are scheduled to be.placed in service with all CEA's fully out of the core except that the lead regulating group, group 6, will be about 110 inches withdrawn. When the CPC's are removed I
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Mr. R. H. Engel ken July 2, 1982 from bypass with this CEA configuration, a CPC trip on DNBR would have been perceived by the CPC's as one of the subgroups in shut-down group A.
Thus, the CPC's would see all rods out except a shutdown subgroup. Penalty factors would be applied because of subgroup deviation and radial peaking. This combined effect would result in a multiplicative penalty factor of approximately 20.
At low powers, the CPC's assume a power level of 20%.
This penalty factor of 20 coupled with the power level of 20% would have guaranteed an immediate reactor trip. There was no impact on health and public safety.
Please contact me if you have further questions concerning this matter.
Sincerely,
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Enclosure:
LER No.80-034 cc:
Mr. A. E. Chaf fee (USNRC Resident inspector, San Onof re Unit 2)
U. S. Nuclear Regulatory Commission Office of inspection and Enforcement U. S. Nuclear Regulatory Commission Of fice of Management Information & Program Control institute of Nuclear Power Operations L
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| 05000361/LER-1982-001-03, /03L-0:on 820214,during Initial Fuel Load,Control Room Emergency Air Cleanup Sys Charcoal Filters (E-419 & A-206) Were Saturated W/Water.Caused by Operator Opening Isolation Valve.Filters Replaced & Sys Returned to Svc | /03L-0:on 820214,during Initial Fuel Load,Control Room Emergency Air Cleanup Sys Charcoal Filters (E-419 & A-206) Were Saturated W/Water.Caused by Operator Opening Isolation Valve.Filters Replaced & Sys Returned to Svc | | | 05000361/LER-1982-001, Forwards LER 82-001/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-001/03L-0.Detailed Event Analysis Submitted | | | 05000361/LER-1982-001-01, /01T-0:on 821128,emergency Chiller E-335 Declared Inoperable,Rendering Creacus Train B Inoperable.Caused by Failure of Resistance Temp Detector in Motor Winding High Temp Trip Circuit.Spare Resistance Temp Detector Installed | /01T-0:on 821128,emergency Chiller E-335 Declared Inoperable,Rendering Creacus Train B Inoperable.Caused by Failure of Resistance Temp Detector in Motor Winding High Temp Trip Circuit.Spare Resistance Temp Detector Installed | | | 05000206/LER-1982-001-01, /01T-0:on 811210,Sigma Instruments Inc Informed of Potential Deficiency in Lumigraph Indicators Model 9270. Caused by Incorrectly Specified Resistors Incorporated Into Indicator Circuits.Replacement Planned for Mar 1982 Outa | /01T-0:on 811210,Sigma Instruments Inc Informed of Potential Deficiency in Lumigraph Indicators Model 9270. Caused by Incorrectly Specified Resistors Incorporated Into Indicator Circuits.Replacement Planned for Mar 1982 Outage | | | 05000206/LER-1982-001, Forwards LER 82-001/01T-0.Detailed Event Analysis Encl | Forwards LER 82-001/01T-0.Detailed Event Analysis Encl | | | 05000361/LER-1982-002-01, /01T-0:on 820314,shutdown Cooling Lost.Caused by Sys Malfunction or Operator Error,Allowing Pressurized Nitrogen to Enter Shutdown Cooling Pump Suction Line When Purification Sys Filter Was Backflushed.Procedures Revised | /01T-0:on 820314,shutdown Cooling Lost.Caused by Sys Malfunction or Operator Error,Allowing Pressurized Nitrogen to Enter Shutdown Cooling Pump Suction Line When Purification Sys Filter Was Backflushed.Procedures Revised | | | 05000206/LER-1982-002-03, /03L-0:on 820128,containment Isolation Valve in Reactor Coolant Letdown line,CV-526,failed to Close on First Two Remote Manual Close Attempts.Caused by Blocking Lever Dropping Insufficiently.Installed Actuators to Be Replace | /03L-0:on 820128,containment Isolation Valve in Reactor Coolant Letdown line,CV-526,failed to Close on First Two Remote Manual Close Attempts.Caused by Blocking Lever Dropping Insufficiently.Installed Actuators to Be Replaced | | | 05000206/LER-1982-002, Forwards LER 82-002/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-002/03L-0.Detailed Event Analysis Submitted | | | 05000362/LER-1982-002-03, /03L-0:on 821119,during Fuel Loading Operations, Water Observed Leaking Through Equipment Hatch Seal Into Containment.Caused by Existing Gap Around Perimeter of Hatch.Bolts Retightened | /03L-0:on 821119,during Fuel Loading Operations, Water Observed Leaking Through Equipment Hatch Seal Into Containment.Caused by Existing Gap Around Perimeter of Hatch.Bolts Retightened | | | 05000362/LER-1982-002, Forwards LER 82-002/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-002/03L-0.Detailed Event Analysis Submitted | | | 05000362/LER-1982-003-03, /03L-0:on 821127,while in Mode 6,channel 2 Startup Monitor 3JI-006 Lost Visual Indication & Declared Inoperable.Caused by Loss of Power When Monitor Control Ctr 3BN Taken Out of Svc.Load Lists Will Be Reviewed | /03L-0:on 821127,while in Mode 6,channel 2 Startup Monitor 3JI-006 Lost Visual Indication & Declared Inoperable.Caused by Loss of Power When Monitor Control Ctr 3BN Taken Out of Svc.Load Lists Will Be Reviewed | | | 05000361/LER-1982-003-01, /01T-0:on 820314,unplanned Dilution of RCS Resulted When Operators Were Trying to Restore Shutdown Cooling Flow.Caused by Two Manual Valves Being Partially Open Simultaneously While One Being Opened & Other Closed | /01T-0:on 820314,unplanned Dilution of RCS Resulted When Operators Were Trying to Restore Shutdown Cooling Flow.Caused by Two Manual Valves Being Partially Open Simultaneously While One Being Opened & Other Closed | | | 05000362/LER-1982-003, Forwards LER 82-003/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-003/03L-0.Detailed Event Analysis Submitted | | | 05000206/LER-1982-003-99, /99X-0:on 811212,control Rod C-7 Stuck During Startup & Was Freed After Repeated Manipulation.Caused by Dropped Rodlets Due to Failure of Weld Attaching Supporting Vane to Rod Cluster Control (RCC) Hub.Rcc to Be Replaced | /99X-0:on 811212,control Rod C-7 Stuck During Startup & Was Freed After Repeated Manipulation.Caused by Dropped Rodlets Due to Failure of Weld Attaching Supporting Vane to Rod Cluster Control (RCC) Hub.Rcc to Be Replaced | | | 05000206/LER-1982-003, Forwards LER 82-003/99X-0.Detailed Event Analysis Submitted | Forwards LER 82-003/99X-0.Detailed Event Analysis Submitted | | | 05000206/LER-1982-004, Provides Addl Info for LER 82-004 Re Injection of Sodium Hypochlorite Into Cooling Water Sys Above Allowable Limit, Initially Reported 820204.Sys Components Found to Function Correctly.Sys Will Be Continuously Monitored | Provides Addl Info for LER 82-004 Re Injection of Sodium Hypochlorite Into Cooling Water Sys Above Allowable Limit, Initially Reported 820204.Sys Components Found to Function Correctly.Sys Will Be Continuously Monitored | | | 05000361/LER-1982-004-03, /03L-0:on 820308,containment Purge Isolation Sys (Cpis) Operability Found Not Demonstrated Per Tech Spec 4.99.Caused by Return of Purge Valves to Svc After Valve Seat Cleaning W/O Verifying Cpis Operability | /03L-0:on 820308,containment Purge Isolation Sys (Cpis) Operability Found Not Demonstrated Per Tech Spec 4.99.Caused by Return of Purge Valves to Svc After Valve Seat Cleaning W/O Verifying Cpis Operability | | | 05000206/LER-1982-004-01, /01T-0:on 820129,chlorine Residual in Circulating Water Sys Exceeded Tech Spec Limits During Normal Operation. Caused by Air Operated Valve Controlling Flow to Circulating Water Sys Failing Closed,While Injection Pump Contin | /01T-0:on 820129,chlorine Residual in Circulating Water Sys Exceeded Tech Spec Limits During Normal Operation. Caused by Air Operated Valve Controlling Flow to Circulating Water Sys Failing Closed,While Injection Pump Continued | | | 05000361/LER-1982-005-03, /03L-0:on 820309,control Room Emergency Air Cleanup Sys Failed to Start Upon Receiving Spurious Toxic Gas Isolation Signal.Caused by Incorrect Positioning of Kirk Key.Caution Notes Incorporated Into Procedures | /03L-0:on 820309,control Room Emergency Air Cleanup Sys Failed to Start Upon Receiving Spurious Toxic Gas Isolation Signal.Caused by Incorrect Positioning of Kirk Key.Caution Notes Incorporated Into Procedures | | | 05000206/LER-1982-005-03, /03L-0:on 820228,during Normal Power Operation, Containment Isolation Valve SV-70ZC Failed to Close on Demand.Possibly Caused by Contaminants in Valve Soft Goods. Solenoid Valve or Soft Goods to Be Replaced | /03L-0:on 820228,during Normal Power Operation, Containment Isolation Valve SV-70ZC Failed to Close on Demand.Possibly Caused by Contaminants in Valve Soft Goods. Solenoid Valve or Soft Goods to Be Replaced | | | 05000206/LER-1982-005, Forwards LER 82-005/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-005/03L-0.Detailed Event Analysis Submitted | | | 05000362/LER-1982-005-03, /03L-0:on 821205,during Mode 5,diesel Generator 3GOO3 Taken Out of Svc Leaving Boration Flow Paths W/O Emergency Power Sources.Caused by Personnel Error Due to Failure to Recognize Consequences.Personnel Counseled | /03L-0:on 821205,during Mode 5,diesel Generator 3GOO3 Taken Out of Svc Leaving Boration Flow Paths W/O Emergency Power Sources.Caused by Personnel Error Due to Failure to Recognize Consequences.Personnel Counseled | | | 05000362/LER-1982-005, Forwards LER 82-005/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-005/03L-0.Detailed Event Analysis Submitted | | | 05000361/LER-1982-006, Forwards LER 82-006/99X-0.Detailed Event Analysis Submitted | Forwards LER 82-006/99X-0.Detailed Event Analysis Submitted | | | 05000362/LER-1982-006, Ro:On 821217,incident Involving Emergency Safety Features Actuation Signal Occurred.Written Followup Rept W/Interim LER 82-006 Will Be Submitted by 821228 | Ro:On 821217,incident Involving Emergency Safety Features Actuation Signal Occurred.Written Followup Rept W/Interim LER 82-006 Will Be Submitted by 821228 | | | 05000206/LER-1982-006-99, /99X-0:on 811120,refueling Water Tank Level Decreased & Sphere Sump Actuation Increased.Caused by Water Leaking Through Containment Spray Block Valves CV-82 & CV-114 Due to Open Isolation Valve | /99X-0:on 811120,refueling Water Tank Level Decreased & Sphere Sump Actuation Increased.Caused by Water Leaking Through Containment Spray Block Valves CV-82 & CV-114 Due to Open Isolation Valve | | | 05000206/LER-1982-006, Forwards LER 82-006/99X-0.Detailed Event Analysis Submitted | Forwards LER 82-006/99X-0.Detailed Event Analysis Submitted | | | 05000361/LER-1982-007, Ro:Submits Corrections to Equipment Tag Number Errors in LER 82-007 on 820407 | Ro:Submits Corrections to Equipment Tag Number Errors in LER 82-007 on 820407 | | | 05000361/LER-1982-007-03, /03L-0:on 820303,cable Riser Shaft Water Spray Fire Protection Sys Inadvertently Activated & Fire Retardant Barrier Matl Damaged by Water.Caused by Personnel Communication Failure During Maint | /03L-0:on 820303,cable Riser Shaft Water Spray Fire Protection Sys Inadvertently Activated & Fire Retardant Barrier Matl Damaged by Water.Caused by Personnel Communication Failure During Maint | | | 05000206/LER-1982-007, Forwards LER 82-007/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-007/03L-0.Detailed Event Analysis Submitted | | | 05000206/LER-1982-007-03, /03L-0:on 820208,south Saltwater Cooling Pump (G13B) Declared Inoperable.Caused by Random Failure of Discharge Pressure switch,PS-39.Pressure Switch Replaced | /03L-0:on 820208,south Saltwater Cooling Pump (G13B) Declared Inoperable.Caused by Random Failure of Discharge Pressure switch,PS-39.Pressure Switch Replaced | | | 05000362/LER-1982-007-03, /03L-0:on 821211,during Mode 5,review of Strip Chart Recordings of RCS Temps During Filling & Venting Operations on 821210 Indicated RCS Heatup Rate Exceeded. Caused by Inadequate Attention to Heatup Restrictions | /03L-0:on 821211,during Mode 5,review of Strip Chart Recordings of RCS Temps During Filling & Venting Operations on 821210 Indicated RCS Heatup Rate Exceeded. Caused by Inadequate Attention to Heatup Restrictions | | | 05000362/LER-1982-007, Forwards LER 82-007/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-007/03L-0.Detailed Event Analysis Submitted | | | 05000361/LER-1982-008-01, /01T-0:on 820324,dilution of 0.7% Reactivity Occurred Due to Addition of 6,732 Gallons of Water from Refueling Water Storage Tank to Rcs,Resulting in 19% Shutdown Margin.Caused by Leaking Flow Valve 2FV-0210X | /01T-0:on 820324,dilution of 0.7% Reactivity Occurred Due to Addition of 6,732 Gallons of Water from Refueling Water Storage Tank to Rcs,Resulting in 19% Shutdown Margin.Caused by Leaking Flow Valve 2FV-0210X | | | 05000362/LER-1982-008-03, /03L-0:on 821215,while in Mode 5,RCS Chloride Level Exceeded Limit of 0.15 Ppm.Caused by Displacement of Chloride from Purification Ion Exchange Resin to Rcs. Resin Replaced | /03L-0:on 821215,while in Mode 5,RCS Chloride Level Exceeded Limit of 0.15 Ppm.Caused by Displacement of Chloride from Purification Ion Exchange Resin to Rcs. Resin Replaced | | | 05000362/LER-1982-008, Forwards LER 82-008/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-008/03L-0.Detailed Event Analysis Submitted | | | 05000206/LER-1982-008, Forwards LER 82-008/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-008/03L-0.Detailed Event Analysis Submitted | | | 05000206/LER-1982-008-03, /03L-0:on 820227,during Performance of Special Engineering Safety Injection Test,Safeguard Load Sequencer Failed to Activate X Subchannel Sys Relays.Caused by Power Transistor Failure.Circuit Card Replaced | /03L-0:on 820227,during Performance of Special Engineering Safety Injection Test,Safeguard Load Sequencer Failed to Activate X Subchannel Sys Relays.Caused by Power Transistor Failure.Circuit Card Replaced | | | 05000361/LER-1982-008, Forwards LER 82-008/01T-0.Detailed Event Analysis Submitted | Forwards LER 82-008/01T-0.Detailed Event Analysis Submitted | | | 05000206/LER-1982-009-01, /01T-0:on 820405,failed Attachment Welds on Four Feedwater Sys Pipe Supports Discovered During Scheduled Insp.Cause Undetermined.Metallurgical & Design Analysis in Progress.Failed Supports Being Replaced | /01T-0:on 820405,failed Attachment Welds on Four Feedwater Sys Pipe Supports Discovered During Scheduled Insp.Cause Undetermined.Metallurgical & Design Analysis in Progress.Failed Supports Being Replaced | | | 05000206/LER-1982-009, Forwards LER 82-009/01T-0.Detailed Event Analysis Submitted | Forwards LER 82-009/01T-0.Detailed Event Analysis Submitted | | | 05000361/LER-1982-009-01, /01T-0:on 820325,Bechtel Informed Util of Location of Lumigraph Indicators Model 9270 Mfg W/Incorrect Resistors in Indicator Circuits.Caused by Improper Design of Indicator Circuits.Resistors to Be Replaced Prior to Full Pow | /01T-0:on 820325,Bechtel Informed Util of Location of Lumigraph Indicators Model 9270 Mfg W/Incorrect Resistors in Indicator Circuits.Caused by Improper Design of Indicator Circuits.Resistors to Be Replaced Prior to Full Power | | | 05000361/LER-1982-010-01, /01T-0:on 820401,during Mode 5 Following Fuel Loading,Fire Barrier Insp Revealed That Earlier Insp Failed to List Breeches in Fire Barries Completely.Caused by Misunderstanding.Personnel Reinstructed | /01T-0:on 820401,during Mode 5 Following Fuel Loading,Fire Barrier Insp Revealed That Earlier Insp Failed to List Breeches in Fire Barries Completely.Caused by Misunderstanding.Personnel Reinstructed | | | 05000361/LER-1982-010-03, Fire Detection Panels in Zones 1,9 & 28 Failed Surveillance Test S023-I-2.62.Caused by Component Failure | Fire Detection Panels in Zones 1,9 & 28 Failed Surveillance Test S023-I-2.62.Caused by Component Failure | | | 05000362/LER-1982-010, Forwards LER 82-010/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-010/03L-0.Detailed Event Analysis Submitted | | | 05000362/LER-1982-010-03, /03L-0:on 821115,during Surveillance Testing,Fire Detection Instrumentation Found Inoperable.Testing Revealed Need to Replace/Repair Parts of Sys.Replacements/Repairs Expected to Be Complete in 90 Days | /03L-0:on 821115,during Surveillance Testing,Fire Detection Instrumentation Found Inoperable.Testing Revealed Need to Replace/Repair Parts of Sys.Replacements/Repairs Expected to Be Complete in 90 Days | | | 05000206/LER-1982-010, Forwards LER 82-010/99X-0.Detailed Event Analysis Submitted | Forwards LER 82-010/99X-0.Detailed Event Analysis Submitted | | | 05000206/LER-1982-010-99, /99X-0:on 820317,three Tubes on Inlet Side of Steam Generator C Found Leaking.Caused by Intergranular Attack at Top of Tubesheet on Tube Portion of tube-sleeve Assembly.Leaking Tubes Removed from Svc by Plugging | /99X-0:on 820317,three Tubes on Inlet Side of Steam Generator C Found Leaking.Caused by Intergranular Attack at Top of Tubesheet on Tube Portion of tube-sleeve Assembly.Leaking Tubes Removed from Svc by Plugging | | | 05000361/LER-1982-010, Forwards LER 82-010/01T-0.Detailed Event Analysis Submitted | Forwards LER 82-010/01T-0.Detailed Event Analysis Submitted | | | 05000362/LER-1982-011, Forwards LER 82-011/03L-0.Detailed Event Analysis Submitted | Forwards LER 82-011/03L-0.Detailed Event Analysis Submitted | |
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