IR 05000397/2019001

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NRC Integrated Inspection Report 05000397/2019001
ML19126A291
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 05/06/2019
From: Mark Haire
NRC/RGN-IV/DRP/RPB-A
To: Sawatzke B
Energy Northwest
References
IR 2019001
Download: ML19126A291 (28)


Text

SUBJECT:

COLUMBIA GENERATING STATION - NRC INTEGRATED INSPECTION REPORT 05000397/2019001

Dear Mr. Sawatzke:

On March 31, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Columbia Generating Station. On April 11, 2019, the NRC inspectors discussed the results of this inspection with Mr. A. Javorik, Vice President of Engineering, and other members of your staff. The results of this inspection are documented in the enclosed report.

NRC inspectors documented one finding of very low safety significance (Green) in this report.

The finding did not involve a violation of NRC requirements.

If you disagree with a cross-cutting aspect assignment or a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the NRC resident inspector at the Columbia Generating Station.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Mark S. Haire, Branch Chief Project Branch A Division of Reactor Projects Docket No. 05000397 License No. NPF-21 Enclosure:

Inspection Report 05000397/2019001 w/attachment: Documents Reviewed

U.S. NUCLEAR REGULATORY COMMISSION

Inspection Report

Docket Number(s): 05000397 License Number(s): NPF-21 Report Number(s): 05000397/2019001 Enterprise Identifier: I-2019-001-0010 Licensee: Energy Northwest Facility: Columbia Generating Station Location: North Power Plant Loop Richland, WA 99354 Inspection Dates: January 1, 2019, to March 31, 2019 Inspectors: G. Kolcum, Senior Resident Inspector L. Merker, Senior Resident Inspector R. Alexander, Senior Project Engineer E. Combs, Project Engineer/Acting Resident Inspector P. Elkmann, Senior Emergency Preparedness Inspector Approved By: Mark S. Haire, Chief Project Branch A Division of Reactor Projects Enclosure

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a Quarterly inspection at Columbia Generating Station in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. Findings being considered in the NRCs assessment are summarized in the table below.

List of Findings and Violations Failure to Enter the Operational Decision-Making Process for a Condition Reducing Operating Margin in Accordance with Station Procedures Cornerstone Significance Cross-cutting Report Aspect Section Initiating Events Green [H.14] - 71111.13 FIN 05000397/2019001-01 Conservative Closed Bias The inspectors identified a Green finding for the licensees failure to adhere to station procedure, Plant Procedures Manual 1.3.67, Operational Decision-Making Process,

Revision 17, Step 6.1, for a condition that creates an actual or potential reduction in operating or design margin. Specifically, the station failed to enter the Operational Decision-Making (ODM) process for degraded startup auxiliary power transformer oil level that reduced operating margin. This resulted in a lockout of the transformer requiring an unplanned entry into Technical Specification 3.8.1, AC Sources - Operating, Condition A for one offsite circuit inoperable and elevation of plant risk level to Orange Risk for emergent maintenance.

Additional Tracking Items Type Issue Number Title Report Status Section LER 05000397/2018001-00 Automatic Reactor Scram Due 71153 Closed to Main Transformer Trip LER 05000397/2018001-01 Automatic Reactor Scram Due 71153 Closed to Main Transformer Trip

PLANT STATUS

The plant began the inspection period at 100 percent rated thermal power.

On January 12, 2019, the unit was down powered to 65 percent to perform a control rod sequence exchange. Reactor power returned to 100 percent on January 13, 2019.

On January 21, 2019, the unit was down powered to 65 percent due to condensate booster pump 2C discharge check valve COND-V-119C leakage. Reactor power returned to 100 percent on January 24, 2019, and remained at or near rated thermal power for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html.

Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515, Appendix D, Plant Status, and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection Impending Severe Weather Sample (IP Section 03.03)

(1) The inspectors evaluated readiness for impending adverse weather conditions for extreme cold weather during the week of February 4, 2019.
(2) The inspectors evaluated readiness for impending adverse weather conditions for winds greater than 30 mph during a snowstorm, on February 9, 2019.

External Flooding Sample (IP Section 03.04) (1 Sample)

The inspectors evaluated readiness to cope with external flooding for the standby service water pump rooms, on February 15, 2019.

71111.04 - Equipment Alignment Partial Walkdown (IP Section 02.01)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) 125V dc system, on January 11, 2019
(2) reactor core isolation coolant system lineup with diesel generator 3 maintenance, on January 28, 2019
(3) seismic monitoring system on February 28, 2019
(4) standby service water system A with standby service water system B inoperability, on March 22, 2019

71111.04S - Equipment Alignment Complete Walkdown (IP Section 02.02)

The inspectors evaluated system configurations during a complete walkdown of the 125/250 VDC breaker lineup system on February 8, 2019.

71111.05Q - Fire Protection Quarterly Inspection (IP Section 03.01)

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) Fire Area RC-4/1: Electrical Equip and RPS Rooms Division 1, on February 8, 2019
(2) Fire Area RC-5/1: Battery and Security Equip Rooms Division 1, on February 15, 2019
(3) Fire Area RC-6/2: Battery Room Division 2, on February 22, 2019
(4) Fire Area RC-7/2: Electrical Equip and RPS Rooms Division 2, on March 1, 2019
(5) Fire Area RC-14, SM-7: Switchgear Room Division 1, on March 18, 2019

71111.06 - Flood Protection Measures Inspection Activities - Internal Flooding (IP Section 02.02a.)

The inspectors evaluated internal flooding mitigation protections in the Division 1 and Division 2 switchgear rooms, on March 8, 2019.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01)

The inspectors observed and evaluated licensed operator performance in the Control Room during a down-power and removal of the 2C condensate booster pump for maintenance on January 21, 2019, and restart of the 2C condensate booster pump on January 24, 2019.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

The inspectors observed and evaluated the licensed operator requalification evaluated scenario (Crew C) on January 14, 2019.

71111.12 - Maintenance Effectiveness Routine Maintenance Effectiveness Inspection (IP Section 02.01)

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

(1) standby service water system A planned maintenance, week of January 7, 2019
(2) condensate booster pump 2C discharge check valve packing leakage, on January 21, 2019
(3) startup transformer lockout due to low oil level, on February 7, 2019
(4) residual heat removal system A pump and motor replacement, on March 29, 2019

71111.13 - Maintenance Risk Assessments and Emergent Work Control Risk Assessment and Management Sample (IP Section 03.01)

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) yellow risk due to standby service water system A planned maintenance, week of January 7, 2019
(2) high risk troubleshooting of control room reactor vessel wide range water level, on January 18, 2019
(3) yellow risk due to diesel generator 3 planned maintenance, week of January 27, 2019
(4) high risk work during lifting and landing leads for scram discharge volume trip transmitter, on February 1, 2019
(5) orange risk due to start up transformer lockout caused by low oil level, on February 7, 2019
(6) high risk lift plan for new fuel receipt, on February 18, 2019
(7) yellow plant risk and blue fire risk due to diesel generator 2 out-of-service for planned major maintenance, on March 18, 2019
(8) yellow risk for standby service water pump 1B maintenance, on March 23, 2019

71111.15 - Operability Determinations and Functionality Assessments Sample Selection (IP Section 02.01)

The inspectors evaluated the following operability determinations and functionality assessments:

(1) diverse and flexible coping strategy (FLEX) components environmental qualifications for site extreme temperatures, on January 15, 2019
(2) reactor level switch MS-LS-300C and reactor level indicating switch MS-LIS-200C operability, on January 18, 2019
(3) main steam isolation valve indication during surveillance, on January 23, 2019
(4) low oil level in startup transformer, on February 7, 2019
(5) diesel generator 1 governor setting, on March 1, 2019
(6) vital island fire detector fault, on March 8, 2019
(7) standby service water pump 1B failure to run, on March 22, 2019

71111.18 - Plant Modifications Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02)

The inspectors evaluated permanent modification Engineering Change (EC) 15891, seismic monitoring system replacement, on March 21, 2019.

71111.19 - Post Maintenance Testing Post Maintenance Test Sample (IP Section 03.01)

The inspectors evaluated the following post maintenance tests:

(1) standby service water pump room fan 1A, on January 7, 2019
(2) standby service water pump A, on January 9, 2019
(3) low-pressure core spray water leg pump, on January 10, 2019
(4) condensate booster pump 2C, discharge check valve packing maintenance run, on January 23, 2019
(5) circulating water pump B, on January 28, 2019
(6) high voltage power supply replacement of intermediate range channel F monitor, on January 29, 2019
(7) rod drive control system post maintenance testing, on February 15, 2019
(8) diesel fire pump leak on coupling during pump run, on February 18, 2019
(9) standby service water pump 1B, on March 23, 2019

71111.22 - Surveillance Testing The inspectors evaluated the following surveillance tests: In Service Testing (IST) (IP Section 03.01)

The inspectors evaluated OSP-SLC/IST-Q701, standby liquid control pumps operability test, on January 15, 2019.

Surveillance Testing (IP Section 03.01) (4 Samples)

(1) PPM OSP-SW-M101, perform standby service water pump A flow balance, on January 8, 2019
(2) OSP-CCH/IST-M701, control room emergency chiller system A operation, on January 9, 2019
(3) OSP-ELEC-M701, diesel generator 1 monthly operation, on January 9, 2019
(4) OSP-ELEC-M702, diesel generator 2 monthly operation, on January 22, 2019

71114.02 - Alert and Notification System Testing Inspection Review (IP Section 02.01-02.04)

The inspectors evaluated the maintenance and testing of the licensee's offsite alert and notification system for the public on January 31, 2019.

71114.03 - Emergency Response Organization Staffing and Augmentation System Inspection Review (IP Section 02.01-02.02)

The inspectors evaluated the staffing and readiness of the licensee's Emergency Preparedness Organization on January 31, 2019.

71114.04 - Emergency Action Level and Emergency Plan Changes Inspection Review (IP Section 02.01-02.03)

The inspectors evaluated the following submitted Emergency Action Level and Emergency Plan changes:

  • EPIP 13.1.1A, "Classifying the Emergency, Technical Bases," Revision 34 This evaluation does not constitute NRC approval.

71114.05 - Maintenance of Emergency Preparedness Inspection Review (IP Section 02.01 - 02.11)

The inspectors evaluated the licensee's maintenance of their emergency preparedness program on January 28 and 29, 2019.

71114.06 - Drill Evaluation Emergency Preparedness (EP) Drill (IP Section 02.01)

The inspectors evaluated the emergency planning drill on February 19,

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators listed below:

IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01) ===

Date Range: January 1, 2018, through December 31, 2018 IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02)

(1 Sample)

Date Range: January 1, 2018, through December 31, 2018 IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 02.03) (1 Sample)

Date Range: January 1, 2018, through December 31, 2018

Drill/Exercise Performance (IP Section 02.12) (1 Sample)

Date Range: January 1, 2018, through December 31, 2018

ERO Drill Participation (IP Section 02.13) (1 Sample)

Date Range: January 1, 2018, through December 31, 2018 Alert & Notification System Reliability (IP Section 02.14) (1 Sample)

Date Range: January 1, 2018, through December 31, 2018

71152 - Problem Identification and Resolution Annual Follow-up of Selected Issues (IP Section 02.03)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) root cause evaluation for the May 18, 2018, reactor scram
(2) evaluation of the December 13, 2018, reactor core isolation cooling system minimum flow valve, RCIC-V-19, trip on thermal overloads

71153 - Followup of Events and Notices of Enforcement Discretion Event Report (IP Section 03.02)

The inspectors evaluated the following Licensee Event Reports (LERs) which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx:

(1) LER 0500397/2018-001-00, Automatic Reactor Scram Due to Main Transformer Trip, on May 18, 2018.

The inspectors determined it was not reasonable to foresee or correct the cause discussed in the LER; therefore, no performance deficiency was identified. The inspectors also concluded that no violation of NRC requirements occurred.

(2) LER 0500397/2018-001-01, Automatic Reactor Scram Due to Main Transformer Trip, on May 18, 2018.

The inspectors reviewed the updated LER submittal. The inspectors determined that it was not reasonable to foresee or correct the cause discussed in the LER; therefore, no performance deficiency was identified. The inspectors also concluded that no violation of NRC requirements occurred.

INSPECTION RESULTS

Failure to Enter the Operational Decision-Making Process for a Condition Reducing Operating Margin in Accordance with Station Procedures Cornerstone Significance Cross-cutting Report Aspect Section Initiating Events Green [H.14] - 71111.13 FIN 05000397/2019001-01 Conservative Closed Bias The inspectors identified a Green finding for the licensees failure to adhere to station procedure, Plant Procedures Manual 1.3.67, Operational Decision-Making Process, Revision 17, Step 6.1, for a condition that creates an actual or potential reduction in operating or design margin. Specifically, the station failed to enter the Operational Decision-Making (ODM) process for degraded startup auxiliary power transformer oil level that reduced operating margin. This resulted in a lockout of the transformer requiring an unplanned entry into Technical Specification 3.8.1, AC Sources - Operating, Condition A for one offsite circuit inoperable and elevation of plant risk level to Orange Risk for emergent maintenance.

Description:

At 4:07 a.m. on February 7, 2019, the plant entered abnormal procedures ABN-Transformer and ABN-Grid after the startup auxiliary power transformer, E-TR-S, locked out on low oil level. An operator in the field reported the oil level out-of-sight low with no observable oil leakage in the vicinity of the transformer.

The licensee determined a significant decrease in oil volume occurred as already sub-freezing outside temperatures dropped an additional 15°F that night. Because the pre-event level was already below the normal operating band, the level change due to temperature was sufficient to lockout the transformer on low oil level.

The inspectors review of the transformer yard logs found that E-TR-S oil level had been consistently recorded through the operating cycle as low in the indicating range, just above the alarm setpoint. Action Reports for alarms received during winter months in previous years indicate that the low temperatures of winter periodically caused the oil volume to shrink to the point of causing an oil level alarm. This phenomenon was a known issue and a nuisance to operators. Those Action Reports were either closed as being complete or closed to trending with no actionable assignments made. Work Requests related to oil addition to the transformer were deferred to the R24 Refueling Outage with the contingency to add oil online.

Plant Procedures Manual (PPM) 1.3.67, Operational Decision-Making (ODM) Process, provides a systematic method for making operational decisions that could significantly challenge plant safety, reduce operating margins, threaten generation, or pose risks to personnel or equipment. It is intended to be performed when there is an actual or potential reduction in operating or design margin. Maintaining the E-TR-S oil level low outside the normal operating band reduced the operating margin by increasing the transformers susceptibility to weather induced level fluctuations with the potential to cause a lockout. Yet, the licensee failed to enter the ODM process to address this reduction in operating margin during the several month period where the transformer oil level was consistently recorded as low. Operators should have entered the ODM process and corrected the low oil level condition to prevent the low temperatures from causing the level to shrink to the point that a transformer low oil level lockout occurred.

Corrective Action(s): The licensee coordinated with Bonneville Power Authority to add oil to E-TR-S. Additional corrective actions include assignments to revise the transformer yard logs to reflect the markings on the level instruments for both startup and backup transformers and to align the methods used by Engineering and Operations to more accurately record and track transformer oil levels.

Corrective Action Reference(s): Action Reports 389753, 389843, 374476, 387608, and 376707

Performance Assessment:

Performance Deficiency: The failure to adhere to station procedures was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it could reasonably be viewed as a precursor to a significant event. The inspectors determined the performance deficiency was more than minor because it adversely affected the Equipment Performance attribute of the Initiating Events cornerstone and its objective to limit the frequency of those events and operations that upset plant stability and challenge critical safety functions, during shutdown as well as power operations. Specifically, the failure to enter a chronic, degraded startup auxiliary power transformer oil level condition that reduced the plant operational margin into the ODM process for tracking and resolution resulted in an unexpected lockout of the transformer on low oil level caused by fluctuation in volume due to cold weather conditions. Loss of the startup auxiliary power transformer resulted in an abnormal electrical distribution and left the backup auxiliary power transformer as the only remaining offsite power source, therefore elevating plant risk level to Orange Risk.

Significance: The inspectors assessed the significance of the finding using Appendix A, Significance Determination of Reactor Inspection Findings for At - Power Situations. Using the questions in Exhibit 1, Initiating Events Screening Questions, the finding was determined to be of very low safety significance (Green) because

(1) the finding did not result in exceeding the reactor coolant system leak rate for a small loss-of-coolant-accident and
(2) did not affect other systems used to mitigate a loss-of-coolant-accident resulting in a total loss of their function.

Cross-cutting Aspect: H.14 - Conservative Bias: Individuals use decision-making-practices that emphasize prudent choices over those that are simply allowable. A proposed action is determined to be safe in order to proceed, rather than unsafe in order to stop. Rather, in this situation the licensee tolerated a degraded condition that reduced operating margin for operational convenience as opposed to identifying the issue as a challenge to plant reliability and entering it into the ODM process for higher visibility, tracking, and resolution.

Enforcement:

Inspectors did not identify a violation of regulatory requirements associated with this finding.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On January 31, 2019, the inspectors presented the results of the emergency preparedness inspection results to Mr. B. Schuetz, Site Vice President, and other members of the licensee staff.
  • On April 11, 2019, the inspectors presented the integrated inspection results for the quarter to Mr. A. Javorik, Vice President of Engineering, and other members of the licensee staff.

DOCUMENTS REVIEWED

71111.01 - Adverse Weather Protection

Procedures

Number Title Revision

1.3.76 Integrated Risk Management 054

ABN-FLOODING Flooding 020

ABN-WIND Tornado/High Winds 032

SOP- Cold Weather Operations

COLDWEATHER- 032

OPS

71111.04 - Equipment Alignment

Procedures

Number Title Revision

ABN- Earthquake

014

EARTHQUAKE

ABN-ELEC- Plant BOP, Div 1,2, & 3 125 VDC Distribution System

015

25VDC Failures

ABN-ELEC- Plant 24VDC Distribution System Failures

005

24VDC

ABN-ELEC- Plant 250VDC Distribution System Failures

004

250VDC

OSP-SW-M101 Standby Service Water Loop A Valve Position Verification 039

SOP-ELEC-125V- 125 VDC System Operation

003

OPS

SOP-ELEC-125V- 125 VDC System Shutdown

003

SHUTDOWN

25 VDC System Start

SOP-ELEC-125V-

009

START

SOP-ELEC-24V- 24 VDC System Operations

004

OPS

VDC System Shutdown

SOP-ELEC-24V-

2

SHUTDOWN

VDC System Start

SOP-ELEC-24V-

003

START

250 VDC System Operations

SOP-ELEC-250V-

2

OPS

SOP-ELEC-250V- 250 VDC System Shutdown

001

SHUTDOWN

SOP-ELEC-250V- 250 VDC Startup of the 250 VDC System

2

START

Miscellaneous

Documents

Number Title Revision

EC 15891 Seismic System Replacement 001

LCS 1.3.7.2 Seismic Monitoring Instrumentation 073

71111.05 - Fire Protection Annual/Quarterly

Procedures

Number Title Revision

1.3.10 Plant Fire Protection Program Implementation 034

1.3.10A Control of Ignition Sources 017

1.3.10B Active Fire System Operability and Impairment Control 016

1.3.10C Control of Transient Combustibles 020

1.3.85 On-Line Fire Risk Management 005

SOP-FP-DRAIN Fire Protection System Drain 001

SOP-FP-FILL Fire Protection System Fill 003

SOP-FP-LU Fire Protection System Valve and Breaker Lineup 009

SOP-FP-OPS Fire Protection System Operations 015

SOP-FP- Fire Protection System Shutdown

006

SHUTDOWN

SOP-FP-START Fire Protection System Startup 006

Miscellaneous

Documents

Number Title Revision

RC-14/1 Pre-Fire Plan: Radwaste 467 Division 1 Switchgear Room 003

71111.06 - Flood Protection Measures

Procedures

Number Title Revision

1.3.57 Barrier Impairment 037

ABN-FLOODING Flooding 020

FSAR-01 Final Safety Analysis Report 064

ISP-FED-X301 ECCS Pump Room Flood Level - Calibration 003

71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance

Procedures

Number Title Revision

3.3.1-QC Reactor Scram Quick Card 001

3.3.1 Reactor Scram 065

5.1.1 RPV Control 021

5.1.3 Emergency RPV Depressurization 021

5.2.1 Primary Containment Control 027

5.3.1 Secondary Containment Control 020

5.5.25 Alternate Injection Using the SLC System 006

13.1.1 Classifying the Emergency 049

13.1.1A Classifying the Emergency Technical Bases 034

ABN-CORE Unplanned Core Operating Conditions 017

ABN-FLOODING Flooding 020

OI-09 Operations Standards and Expectation 070

Miscellaneous

Documents

Number Title Revision

Crew C Evaluated Scenario Cycle 19-1, 4.0 Critique 000

Summary

LR002447 Cycle 19-1 Evaluated Scenario 000

71111.12 - Maintenance Effectiveness

Action Reports

389079 389087 389183 389224 389753

375957 374476 387700

Work Orders

2126449 02084428 02114328 02116386 02087947 02138264 02042797

2072877 29155963

Drawings

Number Title Revision

43-00.84.2 Cast Steel Swing Check Valve ASME Class 600 001

M504-1 Flow Diagram Condensate and Feed Water Systems 111

(Condensate)

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Action Reports

388934 388951 389016 389111 384850

Action Reports

389115 389182 365352 389753 391347

391337 391352

Work Orders

2118830 02138131 02138018 02138019

Procedures

Number Title Revision

1.3.10 Plant Fire Protection Program Implementation 034

1.3.76 Integrated Risk Management 052

1.3.76 Integrated Risk Management 054

1.3.83 Protected Equipment Program 029

ABN-ELEC-GRID Degraded Off Site Power Grid 011

ABN- Transformer Abnormal Operation 024

TRANSFORMER

SOP-ELEC- Removing/Restoring TR-S, From/To Service 006

230KV-OPS

SOP-ELEC- 4160 Volt AC Electrical Power Distribution System Operation 016

4160V-OPS

SWP-MAI-03 Emergent Issue Management 013

71111.15 - Operability Determinations and Functionality Assessments

Action Reports

388768 381457 388934 388951 389016

389111 384850 389115 389182 365352

390459 390460 390461 389753 375957

374476 390732 391347 391337 391352

Work Orders

2118830 02138131 29155963 29147704

Procedures

Number Title Revision

4.603.A7 603.A7 Annunciator Panel Alarms 054

ABN-BKR-FAULT Failure of MOC Switch Activation for Safety Related 002

Breakers

ABN-FSG-002 Water Makeup Strategies for RPV, SFP, DW, WW During an 005

Extended Loss of AC Power or Other Beyond Design Basis

Event

ABN-FSG-002 Water Makeup Strategies for RPV, SFP, DW, WW During an 006

Extended Loss of AC Power or Other Beyond Design Basis

Event

ABN-FSG-002 Water Makeup Strategies for RPV, SFP, DW, WW During an 007

Procedures

Number Title Revision

Extended Loss of AC Power or Other Beyond Design Basis

Event

ABN-SW Service Water Trouble 015

Drawings

Number Title Revision

EWD-15E-045 Electrical Wiring Diagram Reactor Protection System CRD- 003

LT-12C & MS-LT-61C

EWD-15E-017 Electrical Wiring Diagram Reactor Protection System Scram 000

Discharge Volume High Water Level

EWD-15E-47C Electrical Wiring Diagram Reactor Protection System Power 001

Panel RPS-PP-C72/P001 Circuit Detail

71111.18 - Plant Modifications

Action Reports

391305 391308

Procedures

Number Title Revision

13.1.1a Classifying the Emergency - Technical Bases 034

13.14.11 EP Equipment 013

ABN- Earthquake

013

EARTHQUAKE

ABN- Earthquake

014

EARTHQUAKE

ISP-SEIS-X308 Seismic System Channel Calibration 002

Miscellaneous

Documents

Number Title Revision

EC 15891 Seismic System Replacement 001

LCS 1.3.7.2 Seismic Monitoring Instrumentation 073

71111.19 - Post Maintenance Testing

Action Reports

390045 390058 389996 391347 391337

391352

Work Orders

2136285 02117702 02117263 02129637 02129644 02136433 02139024

2138999 02109071

Procedures

Number Title Revision

ISP-IRM-X306 Intermediate Range Monitor Channel F Calibration 012

OSP-LPCS-A702 Low Pressure Core Spray Keep Fill Integrity Test 003

OSP-SW/IST- Standby Service Water Loop B Operability 034

Q702

71111.22 - Surveillance Testing

Work Orders

2129604 02129646 02136285 02130187 02117438

71114.02 - Alert and Notification Systems Testing

Action Reports

360339 360457 366785 368711 369725

371570 372186 372307 373723 384925

385894 388026

Procedures Title Revision

EPIP 13.14.4 4 Emergency Equipment Maintenance and Testing 054

EPI-14 Actions in the event of an Automated Notification System 008

Failure

Miscellaneous

Documents Title Date

Columbia Generating Station Alert and Notification System 11/15/2016

Design Report, Revision 2

Preventative Maintenance Records for Alert and Notification 2018

System Sirens

71114.03 - Emergency Response Organization Staffing and Augmentation

Action Reports

371855 371856 371868

Procedures

Number Title Revision

EPIP 13.4.1 Emergency Notifications 042, 043

EPIP 13.14.9 Emergency Program Maintenance 029

EPI-11 ERO Administration Program 008

Miscellaneous

Documents Title Date

Quarterly Autodialer and Pager Notification Drill Results for

the drill conducted March 11, 2017

Quarterly Autodialer and Pager Notification Drill Results for

the drill conducted May 2, 2017

Quarterly Autodialer and Pager Notification Drill Results for

the drill conducted September 27, 2017

Quarterly Autodialer and Pager Notification Drill Results for

the drill conducted December 12, 2017

Quarterly Autodialer and Pager Notification Drill Results for

the drill conducted March 30, 2018

Quarterly Autodialer and Pager Notification Drill Results for

the drill conducted June 20, 2018

Quarterly Autodialer and Pager Notification Drill Results for

the drill conducted August 21, 2018

Quarterly Autodialer and Pager Notification Drill Results for

the drill conducted December 18, 2018

After Action Report/Improvement Plan for ERO Team B, 02/07/2017

Report for the January 17, 2017, Exercise

After Action Report/Improvement Plan for ERO Team D, 04/24/2017

Report for the March 14, 2017, Exercise

After Action Report/Improvement Plan for ERO Team A, 08/15/2017

Report for the July 18, 2017, Exercise

After Action Report/Improvement Plan for ERO Team C, 11/31/2017

Report for the October 31, 2017, Exercise

After Action Report/Improvement Plan for ERO Team C,

Report for the February 27, 2018, Exercise

After Action Report/Improvement Plan for ERO Team C, 04/24/2018

Report for the March 27, 2018, Exercise

After Action Report/Improvement Plan for ERO Team A,

Report for the May 15, 2018, Exercise

After Action Report/Improvement Plan for ERO Team B,

Report for the July 10, 2018, Exercise

After Action Report/Improvement Plan for ERO Team D,

Report for the September 25, 2018, Exercise

71114.04 - Emergency Plan and Emergency Action Level Changes

No additional documents were reviewed.

71114.05 - Maintenance of Emergency Preparedness

Action Reports

360252 360335 360588 361134 361135

Action Reports

361174 361195 363014 366094 366567

366884 367907 369130 369258 369531

370195 372372 373237 374115 375545

375759 375786 377563 381009 381736

2375 382707 362053 371979 375287

380821 362180 370962 374425 380971

359611

Work Orders

2107621 02083554 02096734 02096731 02103436 02109006 02105740

2121618 02113624 02106177 02098392 02110759 02110805

Procedures

Number Title Revision

EPIP 13.13.2 Emergency Event Termination and Recovery Operations 018

After-Action Reporting 010

Emergency Equipment Maintenance and Testing 018

EPIP 13.14.8 Drill and Exercise Program 018

EPIP 13.14.9 Emergency Program Maintenance 029

EPI-08 Emergency Preparedness Sign Maintenance 005

EPI-11 ERO Administration Program 008

EPI-16 50.54(Q) Change Evaluation 015

EPI-17 After-Action Report/Improvement Plan Formatting, 008

Distribution, and Retention

EPI-21 Drill and Exercise Development and Implementation 018

SWP-ASI-01 Evaluation of Programs, Processes and Suppliers 031

1.3.10 Plant Fire Protection Program Implementation 34-1

Miscellaneous Revision/

Documents Title Date

Columbia Generating Station Emergency Plan 066

After Action Report/Improvement Plan for ERO Team B, 02/07/2017

Report for the January 17, 2017, Exercise

After Action Report/Improvement Plan for ERO Team D, 04/24/2017

Report for the March 14, 2017, Exercise

After Action Report/Improvement Plan for ERO Team A, 08/15/2017

Report for the July 18, 2017, Exercise

After Action Report/Improvement Plan for ERO Team C, 11/31/2017

Report for the October 31, 2017, Exercise

After Action Report/Improvement Plan for ERO Team C,

Report for the February 27, 2018, Exercise

After Action Report/Improvement Plan for ERO Team C, 04/24/2018

Report for the March 27, 2018, Exercise

Miscellaneous Revision/

Documents Title Date

After Action Report/Improvement Plan for ERO Team A,

Report for the May 15, 2018, Exercise

After Action Report/Improvement Plan for ERO Team B,

Report for the July 10, 2018, Exercise

After Action Report/Improvement Plan for ERO Team D,

Report for the September 25, 2018, Exercise

After Action Report for the November 28, 2018, First

Responder Drill (Contaminated/Injured Man)

AU-EP-17 Quality Services Audit Report: Emergency Preparedness 02/23/2017

Program

AU-EP-18 Quality Services Audit Report: Emergency Preparedness 03/12/2018

Program

AU-EP-7 Checklist #8, Offsite Agency Interfaces

2018 Emergency Preparedness Program 12-month Audit 02/05/2018

Frequency Evaluation

Continuous Monitoring Report SR-18-02, Revision 1, 07/05/2018

January through May 2018

Continuous Monitoring Report SR-18-03, June through 10/23/2018

September 2018

2017-03 50.54(q) Screening and Evaluation, , TSC Administrative 02/28/2017

Manager Checklist, Revision 5

2017-16 50.54(q) Screening and Evaluation, EPC 26532, Revision 3 05/02/2017

2017-20 50.54(q) Screening and Evaluation, SWP-EPP-01, 02/06/2018

Revision 22

2017-24 50.54(q) Screening and Evaluation, Cassadian AirBus 08/02/2017

VESTA Communications System Version 5,

2017-25 50.54(q) Screening and Evaluation, EPI-27, Revision 2 09/07/2017

2017-27 50.54(q) Screening and Evaluation, PPM 13.9.1, Revision 09/27/2017

and PPM 13.95, Revision 17

2017-31 50.54(q) Screening and Evaluation, EP Siren Site

Inspections, Revision 1

2018-03 50.54(q) Screening and Evaluation, PPM 13.14.11, 01/09/2018

Revision 13

2018-04 50.54(q) Screening and Evaluation, NRC Liaison Checklist, 01/31/2018

Revision 3, RPM Checklist, Revision 5, and HPN

Communicator Checklist, Revision 1

2018-17 50.54(q) Screening and Evaluation, EAL Technical Bases, 08/14/2018

Revision 34, Emergency Plan 66, and Emergency Event

Termination and Recovery Operations, Revision 18

2018-21 50.54(q) Screening and Evaluation, EOF Manager 06/05/2018

Checklist, Revision 9

2018-32 50.54(q) Screening and Evaluation, EP 2.003, Onshift 06/27/2018

Miscellaneous Revision/

Documents Title Date

Staffing Analysis Report

2018-39 50.54(q) Screening and Evaluation, Plant Administrative 08/28/2018

Manager Checklist, Revision 6

2018-42 50.54(q) Screening and Evaluation, Dose Projection Health 11/13/2018

Physics Checklist, Revision 4

2018-45 50.54(q) Screening and Evaluation, PPM 13.4.1, 10/08/2018

Emergency Notifications, Revision 43-5

2018-46 50.54(q) Screening and Evaluation, PPM 13.8.1, 10/09/2018

Emergency Dose Projection System Operations, Revision

39-1

2018-50 50.54(q) Screening and Evaluation, PPM 13.14.11, 11/08/2018

Revision 1

URI-RASCAL Practice Cases (Draft): January 2019,

April 2019, August 2019, October 2019, December 2019

Just In Time Training Lesson Plan, URI Pathway JITT 08/15/2018

SA370464 Snapshot Self Assessment

SA340626 Focused Self Assessment, Emergency Preparedness

Exercise Year Self Assessment

SA371464 Snapshot Self Assessment 10/25/2018

71114.06 - Drill Evaluation

Procedures

Number Title Revision

13.1.1 Classifying the Emergency 049

13.1.1A Classifying the Emergency-Technical Bases 034

13.10.1 035 004 2/14/2017 Control Room Operation and Shift 035

Manager Duties

13.10.14 Maintenance Manager Duties 009

13.10.16 Chemistry/Effluent Manager Duties 003

13.10.17 TSC Ventilation Radiation Monitor System Operations 005

13.10.2 TSC Manager Duties 035

13.10.3 Technical Manager and Staff Duties 023

13.10.4 Radiation Protection Manager Duties 033

13.10.5 15 Operations Manager Duties 012

13.10.6 Plant / NRC Liaison Duties 025

13.10.7 Plant Administrative Manager Duties 024

13.10.8 Security Lieutenant and Security Force Duties 025

13.10.9 Operations Support Center Manager and Staff Duties 049

13.11.1 EOF Manager Duties 044

Procedures

Number Title Revision

13.11.10 Security Manager Duties 022

13.11.12 EOF Engineering Manager and Staff Duties 031

13.11.2 Assistant EOF Manager Duties 010

13.11.3 Site Support Manager and Staff Duties 032

13.11.7 Radiological Emergency Manager Duties 037

13.12.19 JIC Management 024

13.13.1 Reentry Operations 010

13.13.2 Emergency Event Termination and Recovery Operations 018

71151 - Performance Indicator Verification

Procedures Title

Number Revision

EPIP 13.14.4 Emergency Equipment Maintenance and Testing 054

EPI-18 Emergency Preparedness Performance Indicators 026

EPI-21 Drill and Exercise Development and Implementation 018

71152 - Problem Identification and Resolution

Action Reports

386750 386956 387833 387990 380257

380412 380341 380427 387479

Work Orders

29146086 29146159 29146182 29146189 02049828 02137070 02105341

2128700

Procedures

Number Title Revision

1.3.5 Reactor Trip Report 026

3.3.1 Reactor Scram 064

ABN-RRC-LOSS Loss of Reactor Recirculation Flow 013

ABN-SRV Safety Relief Valve Opening 006

ABN- Transformer Abnormal Operation 022

TRANSFORMER

ESP-MOVTOL- MOV Thermal Overload Testing - CC 022

B301

OSP-RCIC/ RCIC Operability Test 062

IST-Q701

Drawings

Number Title Revision

250-00.47.1 Valve Assembly, 2 inch. Y Type, Globe Valve, Motor

Operated, C.S 000

205-00.17 Generator Step-up Transformer Schematic Diagram 001

Miscellaneous

Documents

Number Title Revision

776-00.1.1 Stack Monitoring System Equipment, Instrumentation, Dual 002

Sum, Amplifier, Power Supply, Modular System and

Coaxicon Vendor Manual

RCIC-MO-19 MOV Master Data Sheet 013

Modifications

Number Title Revision

EC 11288 Replace Stack Monitors 008

Calculations

Number Title Revision

NE-02-09-12 CGS Emergency Action Levels (EALs) Technical Bases 004

NE-02-13-10 Determination of Low Range Stack Monitor Xe-133 000

Equivalent Efficiency

NE-02-15-07 Setpoint Calculation for Reactor Building Elevated 000

Discharge Radiation Monitor (Stack Monitor)

71153 - Follow-up of Events and Notices of Enforcement Discretion

Action Reports

380257 380412 380341 380427

Work Orders

2128700

Procedures

Number Title Revision

1.3.5 Reactor Trip Report 026

3.3.1 Reactor Scram 064

ABN-RRC-LOSS Loss of Reactor Recirculation Flow 013

ABN-SRV Safety Relief Valve Opening 006

ABN- Transformer Abnormal Operation 022

TRANSFORMER

Drawings

Number Title Revision

205-00.17 Generator Step-up Transformer Schematic Diagram 001

ML19126A291

SUNSI Review ADAMS: Non-Publicly Available Non-Sensitive Keyword:

By: Yes No Publicly Available Sensitive NRC-002

OFFICE SRI:DRP/A RI:DRP/C ARI:DRP/A DRS/IPAT DRS/EB1 DRS/EB2

NAME GKolcum LMerker ECombs RKellar VGaddy GPick

SIGNATURE /RA/ /RA/ /RA/ /RA/ /RA/ /RA/

DATE 04/25/2019 4/22/2019 5/1/2019 04/25/2019 4/26/19 4/25/2019

OFFICE DRS/RCB DNMS/RIB DRS/OB SPE:DRP/A BC:DRP/A

NAME NMakris GWarnick GWerner RAlexander MHaire

SIGNATURE /RA/ /RA/ JKatanic /RA/ /RA/ /RA/

for

DATE 04/25/2019 05/01/2019 04/25/2019 04/25/2019 05/6/19