ML16005A567

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IR 05000282/2015008 and 05000306/2015008; 10/05/2015 - 11/24/2015; Prairie Island Nuclear Generating Plant, Units 1 and 2; Annual Problem Identification and Resolution Inspection (Njf)
ML16005A567
Person / Time
Site: Prairie Island  Xcel Energy icon.png
Issue date: 01/05/2016
From: Christine Lipa
NRC/RGN-III/DRS/EB2
To: Davison K
Northern States Power Co
References
IR 2015008
Download: ML16005A567 (30)


See also: IR 05000306/2015008

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION III

2443 WARRENVILLE RD. SUITE 210

LISLE, IL 60532-4352

January 5, 2016

Mr. Kevin Davison

Site Vice President

Prairie Island Nuclear Generating Plant

Northern States Power Company, Minnesota

1717 Wakonade Drive East

Welch, MN 55089

SUBJECT: PRAIRIE ISLAND NUCLEAR GENERATING PLANT, UNITS 1 AND 2 - NRC

ANNUAL FOLLOW-UP OF SELECTED PROBLEM IDENTIFICATION AND

RESOLUTION ISSUES; INSPECTION REPORT 05000282/2015008;

05000306/2015008 AND NOTICE OF VIOLATION

Dear Mr. Davison:

On November 24, 2015, the U.S. Nuclear Regulatory Commission (NRC) completed an annual

problem identification and resolution follow-up sample at your Prairie Island Nuclear Generating

Plant, Units 1 and 2. The enclosed report documents the results of this inspection, which were

discussed on November 24, 2015, with Mr. S. Northam, Vice President of Fleet Operations, and

other members of your staff.

Based on the results of this inspection, the NRC has identified an issue that was evaluated

under the risk significance determination process as having very low safety significance

(Green). The NRC has also determined that a violation is associated with this issue. This

violation was evaluated in accordance with the NRC Enforcement Policy. The current

Enforcement Policy is included on the NRCs web site at (http://www.nrc.gov/about-nrc/

regulatory/enforcement/enforce-pol.html).

This violation is cited in the enclosed Notice of Violation (Notice), and the circumstances

surrounding it are described in detail in the subject inspection report. The violation is being

cited in the Notice, consistent with the NRC Enforcement Policy, Section 2.3.2.a.2, because

Prairie Island Nuclear Generating Plant, Unit 2, failed to restore compliance and failed to have

objective plans to restore compliance in a reasonable time period following the NRC

identification of an associated Non-Cited Violation (NCV) on June 30, 2011. The associated

NCV was documented in Inspection Report (IR) 05000282/2011003; 05000306/2011003.

You are required to respond to this letter and should follow the instructions specified in the

enclosed Notice when preparing your response. If you have additional information that you

believe the NRC should consider, you may provide it in your response to the Notice. The NRC

review of your response to the Notice will also determine whether further enforcement action is

necessary to ensure compliance with regulatory requirements.

Based on the results of this inspection, the NRC has also identified four issues that were

evaluated under the risk significance determination process as having very low safety

significance (Green). The NRC has also determined that violations are associated with these

issues. These violations are being treated as NCVs, consistent with Section 2.3.2 of the

Enforcement Policy. These NCVs are described in the subject inspection report. Additionally,

a licensee-identified violation is listed in Section 4OA7 of this report.

K. Davison -2-

If you contest the subject or severity of any NCVs, you should provide a response within

30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with

copies to the Regional Administrator, Region III; the Director, Office of Enforcement, U.S.

Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident

Inspector at the Prairie Island Nuclear Generating Plant.

In addition, if you disagree with the cross-cutting aspect assigned to any finding in this report,

you should provide a response within 30 days of the date of this inspection report, with the basis

for your disagreement, to the Regional Administrator, Region III, and the NRC Resident

Inspector at Prairie Island Nuclear Generating Plant.

In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public

Inspections, Exemptions, Requests for Withholding, of the NRC's "Rules of Practice," a copy

of this letter, its enclosure, and your response (if any) will be available electronically for public

inspection in the NRCs Public Document Room or from the Publicly Available Records (PARS)

component of the NRC's Agencywide Documents Access and Management System (ADAMS).

ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html

(the Public Electronic Reading Room).

Sincerely,

/RA/

Christine A. Lipa, Chief

Engineering Branch 2

Division of Reactor Safety

Docket Nos. 50-282, 50-306

License Nos. DPR-42, DPR-60

Enclosure:

1. Notice of Violation

2. IR 05000282/2015008; 05000306/2015008

cc: Distribution via LISTSERV

NOTICE OF VIOLATION

Northern States Power Company Docket No. 50-306

Prairie Island Nuclear Generating Plant, Unit 2 License No. DPR-60

During an U.S. Nuclear Regulatory Commission (NRC) inspection conducted from

October 5 through November 24, 2015, a violation of NRC requirements was identified.

In accordance with the NRC Enforcement Policy, the violation is listed below:

Title 10, Code of Federal Regulations (CFR), Part 50, Appendix B, Criterion XVI,

Corrective Action, states, in part, that measures shall be established to assure that

conditions adverse to quality (CAQs), such as failures, malfunctions, deficiencies,

deviations, defective material and equipment, and non-conformances, are promptly

identified and corrected.

Contrary to the above, from April 11, 2011, to at least October 22, 2015, the licensee

failed to correct a CAQ. Specifically, on April 11, 2011, the NRC identified that the

licensee was not monitoring five safety-related gas susceptible locations within the

emergency core cooling system considered to be inaccessible and the licensee

captured this CAQ in their Corrective Action Program. However, on October 22, 2015,

the inspectors identified that the licensee had not corrected this CAQ for two of these

locations and did not have objective plans to restore compliance.

This violation is associated with a Green Significance Determination Process finding.

Pursuant to the provisions of 10 CFR 2.201, Northern States Power Company, is hereby

required to submit a written statement or explanation to the U.S. Nuclear Regulatory

Commission, ATTN: Document Control Desk, Washington, DC 20555-0001 with a copy to

the Regional Administrator, Region III, and a copy to the NRC Resident Inspector at the

Prairie Island Nuclear Generating Plant, Units 1 and 2, within 30 days of the date of the

letter transmitting this Notice. This reply should be clearly marked as a Reply to a Notice of

Violation; VIO 05000306/2015008-01, and should include: (1) the reason for the violation, or,

if contested, the basis for disputing the violation or severity level, (2) the corrective steps that

have been taken and the results achieved, (3) the corrective steps that will be taken, and (4) the

date when full compliance will be achieved. Your response may reference or include previous

docketed correspondence, if the correspondence adequately addresses the required response.

If an adequate reply is not received within the time specified in this Notice, an Order or a

Demand for Information may be issued as to why the license should not be modified,

suspended, or revoked, or why such other action as may be proper should not be taken.

Where good cause is shown, consideration will be given to extending the response time.

If you contest this enforcement action, you should also provide a copy of your response, with

the basis for your denial, to the Director, Office of Enforcement, United States Nuclear

Regulatory Commission, Washington, DC 20555-0001.

Because your response will be made available electronically for public inspection in the NRC

Public Document Room or from ADAMS, accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html, to the extent possible, it should not include any

personal privacy, proprietary, or safeguards information so that it can be made available to the

public without redaction. If personal privacy or proprietary information is necessary to provide

an acceptable response, then please provide a bracketed copy of your response that identifies

Enclosure 1

Notice of Violation

the information that should be protected and a redacted copy of your response that deletes

such information. If you request withholding of such material, you must specifically identify the

portions of your response that you seek to have withheld and provide in detail the bases for your

claim of withholding (e.g., explain why the disclosure of information will create an unwarranted

invasion of personal privacy or provide the information required by 10 CFR 2.390(b) to support

a request for withholding confidential commercial or financial information). If safeguards

information is necessary to provide an acceptable response, please provide the level of

protection described in 10 CFR 73.21.

In accordance with 10 CFR 19.11, you may be required to post this Notice within two working

days of receipt.

Dated this 5th day of January, 2016.

2

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos: 50-282; 50-306

License Nos: DPR-42; DPR-60

Report No: 05000282/2015008; 05000306/2015008

Licensee: Northern States Power Company, Minnesota

Facility: Prairie Island Nuclear Generating Plant, Units 1 and 2

Location: Welch, MN

Dates: October 5 - November 24, 2015

Inspector: N. Féliz Adorno, Senior Reactor Inspector

Approved by: Christine A. Lipa, Chief

Engineering Branch 2

Division of Reactor Safety

Enclosure 2

Table of Contents

SUMMARY ................................................................................................................................ 2

REPORT DETAILS .................................................................................................................... 5

1. REACTOR SAFETY 5

4OA2 Identification and Resolution of Problems (71152) 5

4OA6 Meetings 20

4OA7 Licensee-Identified Violations 20

SUPPLEMENTAL INFORMATION............................................................................................. 1

Key Points of Contact ............................................................................................................. 1

List of Items Opened, Closed and Discussed ......................................................................... 1

List of Documents Reviewed .................................................................................................. 2

List of Acronyms Used ............................................................................................................ 4

SUMMARY

Inspection Report 05000282/2015008, 05000306/2015008; 10/05/2015 - 11/24/2015; Prairie

Island Nuclear Generating Plant, Units 1 and 2; Annual Problem Identification and Resolution

Inspection.

This report covers an 8-week period of inspection by primarily one regional inspector focused on

gas accumulation management in piping. Four Green findings were identified by the inspector

and one Green finding was self-revealed. Four of these findings involved Non-Cited Violations

(NCVs) of U.S. Nuclear Regulatory Commission (NRC) requirements while one of these findings

involved a Notice of Violation of NRC requirements. The significance of inspection findings is

indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red), and determined

using Inspection Manual Chapter (IMC) 0609, Significance Determination Process, dated

April 29, 2015. Cross-cutting aspects are determined using IMC 0310, Aspects Within the

Cross-Cutting Areas, dated December 4, 2014. All violations of NRC requirements are

dispositioned in accordance with the NRCs Enforcement Policy, dated February 4, 2015.

The NRC's program for overseeing the safe operation of commercial nuclear power reactors

is described in NUREG-1649, Reactor Oversight Process, dated February 2014.

NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

  • Green. The inspectors identified a finding of very low safety significance (Green), and

an associated cited violation of Title 10, Code of Federal Regulations (CFR), Part 50,

Appendix B, Criterion XVI, Corrective Actions, for the failure to correct a condition

adverse to quality (CAQ). Specifically, on August 1, 2011, the NRC issued an NCV for

the failure to monitor five safety-related gas susceptible locations considered to be

inaccessible, which is a CAQ. As of November 24, 2015, the licensee had not corrected

this CAQ for two of those locations and did not have plans to restore compliance. The

licensee captured this issue into their Corrective Action Program (CAP) with a proposed

corrective action to develop an alternative monitoring method for these locations when

the unit is operating.

The performance deficiency was determined to be more than minor because it was

associated with the Mitigating Systems cornerstone attribute of equipment performance,

and affected the cornerstone objective of ensuring the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable

consequences. The finding screened as of very low safety significance (Green)

because it did not result in the loss of operability or functionality of mitigating systems.

Specifically, the licensee was able to access and inspect these locations during the

refueling outage that was ongoing when this issue was identified and confirmed that

they were full of water during the previous operating cycle. In addition, a historical

review did not find information that challenged operability due to gas accumulation at

these locations. The inspectors determined that this finding had a cross-cutting

aspect in the area of problem identification and resolution because the licensee did

not thoroughly evaluate their discovery that the CAQ was not been corrected on

July 29, 2013. Specifically, on 2013, the licensee initiated a condition evaluation (CE)

to determine if the action plan at the time addressed the NCV associated with the CAQ.

However, the CE was closed by crediting actions that were similar to those that resulted

in the NCV and other documented observations associated with the inappropriate

resolution of the issue. [P.2] (Section 4OA2.1.c(1))

2

  • Green. The inspectors identified a finding of very low safety significance (Green),

and an associated NCV of 10 CFR Part 50, Appendix B, Criterion V, Instructions,

Procedures, and Drawings, for the licensees failure to manage gas accumulation at

the residual heat removal (RHR) train credited for emergency core cooling in MODE 4,

Hot Shutdown. Specifically, the RHR train credited for emergency core cooling in

MODE 4 was not verified to be full of water before its operability was required in

MODE 4 following system draining during refueling outage 1R29. The licensee

captured this issue into their CAP with a proposed corrective action to revise procedures

to explicitly require these inspections prior to transitioning into MODE 4 during startup

activities.

The performance deficiency was determined to be more than minor because it was

associated with the Mitigating Systems cornerstone attribute of equipment performance,

and affected the cornerstone objective of ensuring the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable

consequences. The finding screened as of very low safety significance (Green)

because it did not result in the loss of operability or functionality of mitigating systems.

Specifically, the licensee reviewed records associated with gas accumulation

management activities during 1R29 and discovered that a non-conforming void was

vented 12 - 18 hours2.083333e-4 days <br />0.005 hours <br />2.97619e-5 weeks <br />6.849e-6 months <br /> after the transition to MODE 4. However, an operability review

reasonably determined that this non-conforming condition did not result in loss of

operability. The inspectors did not identify a cross-cutting aspect associated with this

finding because it was not confirmed to reflect current performance.

(Section 4OA2.1.c(2))

  • Green. A finding of very low safety significance (Green), and an associated NCV of

10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings,

was self-revealed for the licensees failure to establish procedures to verify RHR is

operable with respect to gas accumulation following maintenance outages. Specifically,

procedures were not established to verify the system is sufficiently full of water when

RHR is secured in its standby emergency core cooling system mode of operation during

startup activities following maintenance outages. The licensee captured this issue into

their CAP. As a long term corrective action, the licensee revised procedures to require

gas accumulation inspections of the affected gas susceptible locations as part of the unit

startup activities following a maintenance outage.

The performance deficiency was determined to be more than minor because it was

associated with the Mitigating Systems cornerstone attribute of equipment performance,

and affected the cornerstone objective of ensuring the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable

consequences. The finding screened as of very low safety significance (Green)

because it did not result in the loss of operability or functionality of mitigating systems.

Specifically, the licensee performed a past operability review of the limiting void found at

the RHR piping after maintenance outages and reasonably concluded that the system

remained operable. The inspectors did not identify a cross-cutting aspect associated

with this finding because it was not confirmed to reflect current performance.

(Section 4OA2.1.c(3))

  • Green. The inspectors identified a finding of very low safety significance (Green), and

an associated NCV of 10 CFR Part 50, Appendix B, Criterion III, Design Control, for

the licensees failure to manage potential gas accumulation due to safety injection

3

isolation check valve leakage following maintenance outages. Specifically, the licensee

did not evaluate the potential to accumulate nitrogen at multiple RHR and safety

injection gas susceptible locations due to safety injection check valve unseating caused

by maintenance outages. As a result, the station did not manage this gas intrusion

mechanism. The licensee captured this issue into their CAP with a proposed corrective

action to revise procedures to verify that the safety injection check valves are seated as

part of the unit startup activities following a maintenance outage.

The performance deficiency was determined to be more than minor because it was

associated with the Mitigating Systems cornerstone attribute of equipment performance,

and affected the cornerstone objective of ensuring the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable

consequences. The finding screened as of very low safety significance (Green)

because it did not result in the loss of operability or functionality of mitigating systems.

Specifically, the licensee performed a past operability review of the limiting void found

at one of the affected piping locations and reasonably concluded that the associated

system remained operable. The inspectors did not identify a cross-cutting aspect

associated with this finding because it was not confirmed to reflect current performance.

(Section 4OA2.1.c(4))

  • Green. The inspectors identified a finding of very low safety significance (Green) and

associated NCV of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, for

the licensees failure to identify a continuous gas intrusion into one train of RHR, which

was a CAQ, resulting in a continuous undetected void growth that exceeded the

applicable operability limits. The licensee did not consider applicable active gas

intrusion mechanisms when evaluating the discovery of a void at the RHR piping.

The licensee captured this issue into their CAP and stopped the continuous gas

intrusion into the affected piping location.

The performance deficiency was determined to be more than minor because it was

associated with the Mitigating Systems cornerstone attribute of equipment performance,

and affected the cornerstone objective of ensuring the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable

consequences. The finding screened as of very low safety significance (Green)

because it did not result in the loss of operability or functionality of mitigating systems.

Specifically, the licensee performed a past operability review of the void and reasonably

concluded that the system remained operable. The inspectors determined that this

finding had a cross cutting aspect in the area of human performance because the

licensee did not recognize and plan for the possibility of mistakes when evaluating the

gas surveillance results of February 10, 2015. Specifically, the licensee did not plan for

the possibility that the unacceptable results were indicative of a different problem than

originally determined or a combination of problems. As a result, the licensee failed to

identify the continuous gas intrusion incident. [H.12] (Section 4OA2.1.c(5))

Licensee-Identified Violations

A violation of very low safety significance (Green) that was identified by the licensee has

been reviewed by the NRC. Corrective actions taken or planned by the licensee have

been entered into the licensees CAP. This violation and CAP tracking numbers are

listed in Section 4OA7.

4

REPORT DETAILS

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

4OA2 Identification and Resolution of Problems (71152)

.1 Annual Follow-up of Selected Issues: Management of Gas Accumulation in Piping

a. Inspection Scope

During a review of items entered in the licensees Corrective Action Program (CAP), the

inspectors noted multiple corrective action documents associated with gas accumulation

issues at the residual heat removal (RHR) piping. These issues included the discovery

of unexpected complex gas accumulation issues, unplanned Limiting Condition for

Operation (LCO) entries due to gas accumulation, and gas removal challenges.

The inspectors reviewed selected gas accumulation management issues in light of the

number and complexity of the issues described above against selected performance

attributes contained in Inspection Procedure (IP) 71152-03.06. Specifically, the

inspectors reviewed corrective action documents of selected identified gas accumulation

management problems to assess completeness, accuracy, timeliness, classification,

and prioritization of the problem resolution commensurate with the associated safety

significance. In addition, the inspectors reviewed the associated operability and causal

evaluations, when applicable, to assess the licensee evaluation of non-conforming

conditions and their impact to safe plant operation. The inspectors also reviewed the

licensee consideration of extent of condition and previous occurrences of the associated

problems. In addition, the inspectors reviewed the corrective actions of selected issues

to assess problem resolution activities, including timeliness. This assessment also

included a review of associated drawings, procedures, and design reviews, and

interviews of licensee personnel. The documents reviewed are listed in the Attachment

to this report.

This review constituted one in-depth problem identification and resolution sample as

defined in IP 71152-05.

b. Observations

The inspectors noted the following examples of licensee CAP weaknesses when

addressing gas accumulation management issues:

previously identified, and did not have plans to restore compliance. Specifically,

on August 1, 2011, the U.S. Nuclear Regulatory Commission (NRC) issued a

Non-Cited Violation (NCV) for the failure to monitor five safety-related gas

susceptible locations considered to be inaccessible. As of November 24, 2015,

the licensee had not corrected this CAQ for two of those locations and did not

have plans to restore compliance. The details and enforcement action

associated with this issue are discussed in Section 4OA2.1.c(1) of this Inspection

Report (IR).

5

  • A corrective action associated with a minor violation documented in

IR 05000282/2011003; IR 05000306/2011003, dated August 1, 2011, was

inconsistently implemented. Specifically, on 2011, the inspectors identified

a minor violation of Title 10, Code of Federal Regulations (CFR), Part 50,

Appendix B, Criterion V, Instruction, Procedures, and Drawings, for the failure

to trend the sizes of voids discovered during periodic gas monitoring activities,

which was contrary to procedure H64, Gas Accumulation Management Program

(GAMP). The licensee captured this issue in their CAP as Action Request

(AR) 1271024, and implemented corrective actions to trend void sizes. However,

during this inspection period, the inspectors noted that the licensee inconsistently

trended void sizes. Specifically, void sizes were not clearly documented to

differentiate between the as-found and as-left measurements. In addition, after

the original corrective action was implemented, the licensee implemented a new

trending tool but the data had not been completely uploaded. This inconsistent

implementation of the GAMP trending requirements was determined to be minor

during this inspection period because the data was retrievable and the inspectors

did not find an adverse unrecognized trend. The licensee capture this concern in

their CAP as AR 01496191.

  • The licensee did not document the discovery of a problem in their CAP.

Specifically, during the reactor unit startup activities associated with refueling

outage 1R29, the licensee discovered a void at the RHR system that exceeded

its operability limits when this system was required to be operable. However, the

licensee did not document this CAQ in their CAP. The details and enforcement

action of the associated issue are discussed in Section 4OA2.1.c(2) of this IR.

  • The licensee did not identify a CAQ. Specifically, when evaluating the discovery

of voids at the RHR piping during a surveillance, the licensee did not consider

that the affected locations were vulnerable to active gas intrusion mechanisms

(i.e., those that result in a continuous gas intrusion). As a result, the licensee

failed to identify an ongoing continuous gas intrusion into the RHR system, which

was a CAQ, and the corrective actions taken were limited to address the portion

of the problem that was not associated with the active gas intrusion incident. The

details and enforcement action of this issue are discussed in Section 4OA2.1.c(5)

of this IR, while Sections 4OA2.1.c(3) and 4OA2.1.c(4) discuss the details and

enforcement actions of other closely related issues.

c. Findings

(1) Failure to Correct an Non-Cited Violation Associated with Inadequate Gas Monitoring of

Inaccessible Residual Heat Removal Gas Susceptible Locations

Introduction: A finding of very low safety significance (Green), and an associated

cited violation of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Actions, was

identified by the inspectors for the licensees failure to correct a CAQ. Specifically, on

August 1, 2011, the NRC issued an NCV for the failure to monitor five safety-related

gas susceptible locations considered to be inaccessible, which is a CAQ. As of

November 24, 2015, the licensee had not corrected this CAQ for two of those locations

and did not have plans to restore compliance.

Description: On January 11, 2008, the NRC requested each Generic Letter

(GL) 2008-01, Managing Gas Accumulation in Emergency Core Cooling (ECCS), Decay

Heat Removal (DHR), and Containment Spray (CS) Systems, addressee to evaluate

6

the ECCS, DHR, and CS systems licensing basis, design, testing, and corrective actions

to ensure that gas accumulation was maintained less than the amount that would

challenge the operability of these systems. One of the licensees original actions to

address these requests was to establish procedure H64 to programmatically control gas

accumulation at the Generic Letter (GL) 2008-01 subject systems. Section 4.5.4.B of

procedure H64, Revision 2, stated that, Monitoring may not be practical for locations

that are inaccessible due to radiological, environmental conditions, the plant

configuration or personnel safety. It further stated that For these locations alternative

methods should be developed to monitor the potential void locations. Revision 16 of

procedure FP-G-DOC-05, Procedure Writers Guide, Section 4.12, states that, When

used in NSPM documents, use of the term should denotes an expected action. It also

stated that, Deviations from these expectations require prior management approval.

On April 11, 2011, the NRC identified that the licensee had not developed alternative

methods to monitor the potential for gas accumulation at five inaccessible susceptible

locations that require periodic monitoring (i.e., gas susceptible locations 2RH-13,

2RH-15, 2SI-45, 1SI-41, and 1RH-21). This procedure H64 deviation did not receive

prior management approval as required by procedure FP-G-DOC-05. This issue was

originally captured by the licensee in their CAP as AR 01271826, and was documented

by the inspectors as NCV 05000282/2011003-09; 05000306/2011003-09, Alternative

Methods Were Not Developed for Monitoring Inaccessible Susceptible Locations, in

IR 05000282/2011003; IR 05000306/2011003, dated August 1, 2011. This IR also

documented that the inspectors noted that AR 01271826 was not appropriate for the

issue and were concerned that this vulnerability could result in the cancelation of the

corrective action assignment related to this issue. As a result, the IR stated that the

licensee issued a different corrective action document (i.e., AR 01281682) to capture

this issue.

On July 29, 2013, the licensee discovered that the resolution of AR 01281682 was

effectively a repeat of the inappropriate action associated with AR 01271826 that had

been documented in the IR. Specifically, AR 01281682 was closed to no action by

crediting resolution of a third corrective action document (i.e., AR 01281652). To

resolve the inspectors concerns, the apparent cause evaluation (ACE) conducted

under AR 01281652 credited existing corrective action assignments tracked by

AR 01271826, which was the original corrective action document determined to be

inappropriate to address this concern. The licensee captured this discovery in their CAP

as AR 01391787, and initiated a CE to determine if the action plan at the time addressed

the NCV.

During this inspection period, the inspectors noted that, for Unit 2 RHR gas susceptible

locations 2RH-13 and 2RH-15, the CE was closed by crediting some actions that were

similar to the NRC observations documented in the previous IR associated with

AR 01271826, and with the licensee observations captured in AR 01391787.

Specifically, the CE determined that the closure of AR 01281682 to AR 01281652 was

appropriate because both ARs had the same severity level. However, the CE failed to

recognize that AR 01281652 credited AR 01271826, which had a lower severity level

and was the subject of previous documented concerns. In addition, the inspectors noted

that the CE was closed by crediting other actions that were similar to the actions that

resulted in the NCV. Specifically, the CE determined that the NCV was resolved by

noting that gas susceptible locations 2RH-13 and 2RH-15 were added to the quarterly

gas accumulation surveillance procedures and have been tested by recent surveillances.

7

However, the CE failed to recognize that these locations were always identified by these

procedures but, since these high points were inaccessible, some of the surveillances

were completed at the highest accessible locations and these were not adequate

monitoring locations because they would not allow the detection of voids before they

exceed the applicable design limits. This was the observation that led to the NRC

identification of the NCV in 2011.

The inspectors were concerned because, as of October 22, 2015, the licensee had

not restored compliance and did not have objective plans to restore compliance in a

reasonable time period following the NRC identification of the NCV on April 11, 2011.

The licensee captured the inspectors concerns in the CAP as AR 01498169. The

proposed corrective action to restore compliance at the time of this inspection was to

develop an alternative monitoring method for these locations when the unit is operating.

In addition, since these locations are accessible during outages and the affected unit

was in an outage when this issue was identified, the licensee confirmed that the affected

locations were full of water during the previous operating cycle.

Analysis: The inspectors determined that the failure to correct the lack of periodic gas

accumulation monitoring of inaccessible RHR gas susceptible locations, which is a CAQ,

was contrary to 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, and was

a performance deficiency. The performance deficiency was determined to be more than

minor because it was associated with the Mitigating Systems cornerstone attribute of

equipment performance, and affected the cornerstone objective of ensuring the

availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences. Specifically, the failure to periodically monitor gas

susceptible locations 2RH-13 and 2RH-15 does not ensure the availability and reliability

of the RHR system to perform its accident mitigating function because a potential

adverse void would not be detected and managed to ensure operability.

The inspectors determined the finding could be evaluated using the Significance

Determination Process (SDP) in accordance with Inspection Manual Chapter (IMC) 0609, SDP, Attachment 0609.04, Initial Characterization of Findings, issued

on June 19, 2012. Because the finding impacted the Mitigating Systems cornerstone,

the inspectors screened the finding through IMC 0609, Appendix A, The SDP for

Findings At-Power, issued on June 19, 2012, using Exhibit 2, Mitigating Systems

Screening Questions. The finding screened as of very low safety significance (Green)

because it did not result in the loss of operability or functionality of mitigating systems.

Specifically, the licensee was able to inspect these locations during the refueling outage

that was ongoing when this issue was identified and confirmed that they were full of

water during the previous operating cycle. In addition, a historical review did not find

information that challenged operability due to gas accumulation at these locations.

The inspectors determined that this finding had a cross cutting aspect in the area of

problem identification and resolution because the licensee did not thoroughly evaluate

their discovery that the CAQ was not been corrected on July 29, 2013. Specifically, the

licensee initiated a CE to determine if the action plan at the time addressed the NCV

associated with the CAQ. However, the CE was closed by crediting actions that were

similar to those that resulted in the NCV and other documented observations associated

with the inappropriate resolution of the issue. [P.2]

8

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action,

states, in part, that measures shall be established to assure that CAQs, such as failures,

malfunctions, deficiencies, deviations, defective material and equipment, and

non-conformances, are promptly identified and corrected.

Contrary to the above, from April 11, 2011, to at least October 22, 2015, the licensee

failed to correct a CAQ. Specifically, on April 11, 2011, the NRC identified that the

licensee was not monitoring five safety-related gas susceptible locations within the

ECCS considered to be inaccessible and the licensee captured this CAQ in their CAP.

However, on October 22, 2015, the inspectors identified that the licensee had not

corrected this CAQ for two of these locations and did not have objective plans to

restore compliance.

The licensee is still evaluating its planned corrective actions. However, the inspectors

determined that the continued non-compliance does not present an immediate safety

concern because the affected unit was in an outage and the licensee established

procedures to mitigate the applicable gas intrusion mechanisms during startup activities.

This violation is being cited as described in the Notice, which is enclosed with this IR.

This is consistent with the NRC Enforcement Policy, Section 2.3.2.a.2, which states,

in part, that the licensee must restore compliance within a reasonable period of time

(i.e., in a timeframe commensurate with the significance of the violation) after a violation

is identified. The NRC identified the original issue on April 11, 2011, and dispositioned it

as NCV 05000282/2011003-09; 05000306/2011003-09 in IR 05000282/2011003;

IR 05000306/2011003, dated August 1, 2011. On October 22, 2015, the inspectors

determined that the licensee failed to restore compliance within a reasonable time for

two of the five affected gas susceptible locations following the identification of this CAQ

and failed to have objective plans to restore compliance. (VIO 05000306/2015008-01,

Failure to Correct an NCV Associated with Inadequate Gas Monitoring of Inaccessible

RHR Gas Susceptible Locations)

(2) Failure to Manage Gas Accumulation at the Residual Heat Removal Train Credited for

Emergency Core Cooling in MODE 4

Introduction: The inspectors identified a finding of very low safety significance (Green),

and an associated NCV of 10 CFR Part 50, Appendix B, Criterion V, Instructions,

Procedures, and Drawings, for the licensees failure to manage gas accumulation

at the RHR train credited for emergency core cooling in MODE 4, Hot Shutdown.

Specifically, the RHR train credited for emergency core cooling in MODE 4 was not

verified to be full of water before its operability was required in MODE 4 following

system draining during refueling outage 1R29.

Description: During refueling outage 1R29, which occurred during the fall of 2014,

the licensee partially drained both RHR trains for maintenance work under clearance

orders 56788 and 59050. Subsequently, the drained piping sections were filled and

vented. In addition, the licensee performed dynamic venting in an attempt to flush any

remaining void while in MODE 6, Refueling. While in MODE 5, Cold Shutdown,

some of the gas susceptible locations were inspected to verify that they were full of

water prior to entry into MODE 4 to support the emergency core cooling RHR mode of

operation. Specifically, LCO 3.5.3, ECCS - Shutdown, of the licensees Technical

Specifications (TS) required one ECCS train to be operable in MODE 4 when both

9

reactor coolant system (RCS) cold leg temperatures are greater than the safety

injection pump disable temperature specified in the Pressure and Temperature

Limits Report (PTLR).

During this inspection period, the inspectors noted that the licensee did not inspect all

of the gas susceptible locations that were potentially impacted by the draining activity

prior to crediting the Unit 1 B RHR train for emergency core cooling in MODE 4.

Specifically, the licensee completed these inspections following entry into MODE 4.

In addition, inspection of the Unit 1 B RHR train minimum flow line discovered a

29.1 cubic inch void that exceeded the 18 cubic inch operability limit established in

procedure TP 1468, Unit 1 GL-08-01 Inspections. The licensee estimated that this

discovery occurred 12 - 18 hours2.083333e-4 days <br />0.005 hours <br />2.97619e-5 weeks <br />6.849e-6 months <br /> after transitioning to MODE 4. The Unit 1 A RHR

train was inoperable during this timeframe due to other planned activities.

In addition, the licensee did not capture the discovery of the 29.1 cubic inch void in

their CAP during 1R29. The likely reasons for the failure to initiate a corrective action

document were that the performers of TP 1468 did not recognize that operability of the

affected RHR train was required in MODE 4 and that the as-left condition was within

acceptable limits. As a result, the inspectors reviewed the upcoming refueling outage

schedule and noted that it specified completion of the gas accumulation inspections prior

to transitioning to MODE 4. In addition, the licensee was planning to revise procedure

H64 to explicitly require these inspections prior to MODE 4. However, the inspectors

noted that this revision was not tracked as a corrective action. As a result, the licensee

initiated AR 01496254 to track this procedure revision.

The licensee captured the failure to manage gas accumulation at the RHR train credited

for emergency core cooling in MODE 4 during 1R29 in the CAP as AR 01500190. The

immediate corrective action was to evaluate RHR operability. Specifically, the licensee

determined that the RHR was full of water based on the most recent TP 1468 results.

In addition, the licensee determined that the 29.1 cubic inch void was bounded by recent

operability evaluations of larger voids at the affected location. The proposed plan to

restore compliance at the time of this inspection credited the AR 01496254 assignment

to revise procedure H64.

Analysis: The inspectors determined that the failure to manage gas accumulation for the

RHR train credited for emergency core cooling in MODE 4 was contrary to procedure

H64 and was a performance deficiency. The performance deficiency was determined

to be more than minor because it was associated with the Mitigating Systems

cornerstone attribute of equipment performance and affected the cornerstone objective

of ensuring the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences. Specifically, the failure to manage gas

accumulation for the RHR train credited for emergency core cooling in MODE 4 does not

ensure the availability and reliability of the RHR system to perform its accident mitigating

function. In addition, this failure resulted in crediting an RHR train for emergency core

cooling in MODE 4 that was not verified to be full of water and that was later determined

to have a void that exceeded the associated design limits.

The inspectors determined the finding could be evaluated using the SDP in accordance

with IMC 0609, SDP, Attachment 0609.04, Initial Characterization of Findings, issued

on June 19, 2012. Because the finding occurred during shutdown operations, the

inspectors screened the finding through IMC 0609 Appendix G, Shutdown Operations

10

SDP, issued on May 9, 2014, which referred to Attachment 1 of IMC 0609, Appendix G,

Phase 1 Initial Screening and Characterization of Findings, issued on May 9, 2014.

Because the finding impacted the Mitigating Systems cornerstone, the inspectors

screened the finding through using Exhibit 3, Mitigating Systems Screening Questions,

of this attachment. The finding screened as of very low safety significance (Green)

because it did not result in the loss of operability or functionality of mitigating systems.

Specifically, the licensee reviewed records associated with gas accumulation

management activities during 1R29 and discovered that a non-conforming void was

vented 12 - 18 hours2.083333e-4 days <br />0.005 hours <br />2.97619e-5 weeks <br />6.849e-6 months <br /> after the transition to MODE 4. However, an operability review

reasonably determined that this non-conforming condition did not result in loss of

operability.

The inspectors did not identify a cross-cutting aspect associated with this finding

because it was not confirmed to reflect current performance. Specifically, although

this finding occurred within the last 3 years, the inspectors reviewed the schedule

for the upcoming refueling outage and noted that it specified completion of the gas

accumulation inspections prior to transitioning to MODE 4. In addition, the licensee

was planning to revise procedure H64 to explicitly require these inspections prior to

MODE 4.

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,

and Drawings, requires, in part, that activities affecting quality be prescribed by

documented procedures of a type appropriate to the circumstances and be

accomplished in accordance with these procedures.

The licensee established Revision 2 of procedure H64 as the implementing procedure

for managing gas accumulation in ECCS. Section 4.8 of procedure H64 states that,

Any system maintenance activity that will result in a reduction in fluid inventory of a fluid

system in the scope of the gas accumulation management program should be evaluated

to determine the required fill, vent and verification inspection. It also stated that, The

work processes should include provision for engineering review and evaluation of such

evolutions. Subsection 4.8.3, stated that, Engineering should either specify as part

of their review or confirm the procedure that the selected verification locations will

demonstrate that the system is sufficiently full to perform its functions. It further stated

that, This includes the specification of appropriate verification locations and methods.

The licensee established Revision 16 of procedure FP-G-DOC-05, Procedure

Writers Guide, as the implementing procedure for writing procedures to ensure that

management expectations regarding responsibilities and methods for accomplishing

these responsibilities are provided to personnel. Procedure FP-G-DOC-05,

Section 4.12, states that, When used in NSPM documents, use of the term should

denotes an expected action. It also stated that, Deviations from these expectations

require prior management approval.

Contrary to the above, on November 16, 2014, the licensee failed to follow Section 4.8

of procedure H64. Specifically, the licensee did not specify or confirm that selected

verification locations for RHR demonstrated that the system was sufficiently full of

water to perform its emergency core cooling function in MODE 4 following a system

maintenance activity that resulted in a fluid inventory reduction. In addition, this

deviation did not receive prior management approval, as required by Section 4.12

of procedure FP-G-DOC-05.

11

The licensee is still evaluating its planned corrective actions. However, the inspectors

determined that the continued non-compliance does not present an immediate safety

concern because the licensee created an action to ensure that the upcoming outage

schedule is updated to address this issue.

Because this violation was of very low safety significance and was entered into the

licensees CAP as AR 01500190 and AR 01496254, this violation is being treated as

a NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000282/

2015008-02;05000306/2015008-02, Failure to Manage Gas Accumulation at the RHR

Train Credited for Emergency Core Cooling in MODE 4)

(3) Failure to Establish Procedures to Verify Residual Heat Removal is Full of Water

Following Maintenance Outages

Introduction: A finding of very low safety significance (Green), and an associated NCV

of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings,

was self-revealed for the licensees failure to establish procedures to verify RHR is

operable with respect to gas accumulation following maintenance outages. Specifically,

procedures were not established to verify the system is full of water when RHR is

secured in its standby ECCS mode of operation during startup activities following

maintenance outages.

Description: On December 10, 2014, the licensee began a Unit 1 maintenance outage

associated with a reactor coolant pump (RCP) seal replacement. During this

maintenance outage, the licensee operated RHR in its shutdown cooling mode of

operation, which circulates RCS water through the RHR system. This water had

dissolved nitrogen. On December 24, 2014, the licensee secured shutdown cooling and

aligned both RHR trains for the ECCS mode of operation. This maintenance outage

concluded on December 26, 2014. The licensee did not perform gas accumulation

inspections of the RHR piping to verify it was full of water before declaring it operable for

its ECCS mode of operation. TS LCO 3.5.3 required one ECCS train to be operable in

MODE 4 when both RCS cold leg temperatures are greater than the safety injection

pump disable temperature specified in the PTLR. In addition, TS LCO 3.5.2, ECCS -

Operating, requires two ECCS trains to be operable in MODEs 1, 2, and 3.

On January 26, 2015, the licensee began a second Unit 1 maintenance outage

associated with another RCP seal replacement. Again, the Unit 1 B RHR train was

operated in its shutdown cooling mode circulating nitrogen-rich water throughout its

piping system. On February 9, 2015, the licensee secured shutdown cooling, aligned

the Unit 1 B RHR train for the ECCS mode of operation, and transitioned to MODE 4

and 3. Again, the licensee did not perform gas accumulation inspections of the RHR

piping to verify it was full of water before declaring it operable for its ECCS mode of

operation.

On February 9, 2015, the licensee also began quarterly gas accumulation inspections

using procedure TP 1468. This periodic inspection began after transitioning to MODE 3

and was not part of the unit startup readiness activities following the maintenance

outage. On February 10, 2015, the licensee discovered voids at RHR gas susceptible

locations 1RH-12 and 1RH-11. The 1RH-12 void size was 350 cubic inches, which

exceeded the TP 1468 operability limit of 22.85 cubic inches. The 1RH-11 void size was

62.21 cubic inches, which exceeded the TP 1468 operability limit of 11.62 cubic inches.

The licensee declared both RHR trains inoperable while in MODE 1. The licensee

12

reduced the void sizes below the operability limits by venting these locations later that

day. Location 1RH-12 is downstream of ECCS injection valve MV-32065 at the Unit 1

B RHR train. Location 1RH-11 is a similar location at the Unit 1 A RHR train

downstream of ECCS injection valve MV-32064. These locations are isolated from

the shutdown cooling configuration by these valves, which are open during the ECCS

alignment.

The licensee captured the discovery of these voids in their CAP as AR 01465572 and

performed an ACE. One of the apparent causes was changes in nitrogen solubility.

Specifically, the RHR system introduced water with dissolved nitrogen during shutdown

cooling operations during the maintenance outages and a portion of this nitrogen came

out of solution due to system depressurization when secured for ECCS mode of

operation. The affected locations were system high points and were not verified to

be full of water before exiting the maintenance outages because the procedures

established to perform this verification were not applicable following maintenance

outages. The other apparent cause associated with this problem is discussed further in

Section 4OA2.1.c(5) of this IR. Because the time that the void exceeded the applicable

operability limit remained undetermined during this inspection period, the inspectors

were unable to verify if the licensee appropriately changed MODE during reactor unit

startup activities.

Procedure H64, Section 4.9, Gas Monitoring, stated that, The monitoring plan must

be developed to ensure the system meets the design limit and must ensure the system

is capable of performing its design function throughout the next monitoring interval.

It further stated that, The monitoring frequency for each location requiring periodic

monitoring should be documented in station procedures. It also stated that this

frequency should consider Probability of gas intrusion due to normal plant maneuvers

and equipment manipulation. However, the monitoring frequency for the affected

locations did not consider the system configuration and operational changes

experienced during maintenance outages that can lead to gas accumulation beyond

the system design and operability limits.

The licensees long term corrective actions included a revision of procedures

1/2C1.2-M4, Unit 1/2 Startup to MODE 4, to require gas accumulation inspections of

the affected gas susceptible locations as part of the unit startup activities following a

maintenance outage. In addition, the licensee performed a past operability evaluation

and reasonably determined that the RHR trains remained operable.

Analysis: The inspectors determined that failure to establish procedures to verify RHR is

operable with respect to gas accumulation following maintenance outages was contrary

to 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings,

and was a performance deficiency. The performance deficiency was determined to be

more than minor because it was associated with the Mitigating Systems cornerstone

attribute of equipment performance and affected the cornerstone objective of ensuring

the availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences. Specifically, the failure to have procedures to

verify RHR is full of water following maintenance outages creates the potential for an

unacceptable void to go undetected affecting the availability and capability of this system

to perform the mitigating function.

13

The inspectors determined the finding could be evaluated using the SDP in accordance

with IMC 0609, SDP, Attachment 0609.04, Initial Characterization of Findings.

Because the finding impacted the Mitigating Systems cornerstone, the inspectors

screened the finding through IMC 0609, Appendix A, The SDP for Findings At-Power,

using Exhibit 2, Mitigating Systems Screening Questions. The finding screened as of

very low safety significance (Green) because it did not result in the loss of operability

or functionality of mitigating systems. Specifically, the licensee performed a past

operability review of the void found at 1RH-12 and reasonably concluded that the

system remained operable. The consequence of this void bounded all of the RHR

voids known during this inspection period for the last year.

The inspectors did not identify a cross-cutting aspect associated with this finding

because it was not confirmed to reflect current performance due to the age of the

performance deficiency. Specifically, the procedures associated with gas accumulation

management were developed as part of the GL 2008-01 effort which was completed

more than 3 years ago.

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,

and Drawings, requires, in part, that activities affecting quality be prescribed by

documented procedures of a type appropriate to the circumstances and be

accomplished in accordance with these procedures.

Contrary to the above, as of August 4, 2015, the licensee failed to have procedures

for verifying that RHR was operable as part of the unit startup activities following a

maintenance outage. Specifically, this system experience configuration and operational

changes during maintenance outages that can lead to gas accumulation beyond the

system design and operability limits. However, the procedures failed to verify that the

RHR was sufficiently full of water after RHR was aligned in its standby ECCS mode of

operation during startup activities following maintenance outages.

The licensee is still evaluating its planned corrective actions. However, the inspectors

determined that the continued non-compliance does not present an immediate safety

concern because the licensee vented the nitrogen that accumulated at locations 1RH-11

and 1RH-12.

Because this violation was of very low safety significance and was entered into the

licensees CAP as AR 014465572, this violation is being treated as a NCV, consistent

with Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000282/2015008-03;

05000306/2015008-03, Failure to Establish Procedures to Verify RHR is Full of Water

Following Maintenance Outages)

(4) Failure to Manage Potential Gas Accumulation Due to Safety Injection Isolation Check

Valve Leakage Following Maintenance Outages

Introduction: The inspectors identified a finding of very low safety significance (Green),

and an associated NCV of 10 CFR Part 50, Appendix B, Criterion III, Design Control,

for the licensees failure to manage potential gas accumulation due to safety injection

isolation check valve leakage following maintenance outages. Specifically, the

GL 2008-01 design reviews did not evaluate the potential to accumulate nitrogen at

multiple RHR and safety injection gas susceptible locations due to safety injection check

valve unseating caused by maintenance outages. As a result, the station did not

manage this gas intrusion mechanism.

14

Description: On January 11, 2008, the NRC requested each GL 2008-01 addressee

to evaluate the ECCS, DHR, and CS systems licensing basis, design, testing, and

corrective actions to ensure that gas accumulation was maintained less than the amount

that would challenge the operability of these systems. One of the licensees original

actions to address these requests was to perform design reviews to identify gas

susceptible locations and their applicable gas intrusion mechanisms to manage gas

accumulation at these locations.

On February 24, 2011, the licensee identified that these design reviews were not

documented. Specifically, the licensee did not have quality records documenting

the evaluation of gas susceptible locations that determined which locations required

periodic monitoring. The licensee captured this issue in their CAP as AR 01272406.

This issue was documented as a licensee-identified NCV of 10 CFR Part 50,

Appendix B, Criterion XVII, Quality Assurance Records, in NRC IR 05000282/2011003;

IR 05000306/2011003, dated August 1, 2011. The licensee credited AR 01281652 to

resolve the concern captured in AR 01272406 and, ultimately, AR 01281652 credited a

corrective action assignment under AR 01271580 to resolve this concern. As a result,

on June 9, 2011, the licensee completed their evaluation and documentation of, in part,

specific gas intrusion mechanisms for each identified gas susceptible location.

One of the gas intrusion mechanisms evaluated by the licensee was the introduction of

nitrogen-rich water to the ECCS due to RCS leakage past the safety injection isolation

check valves and subsequent out-gassing due to the reduction of temperature and

pressure at the ECCS piping. This evaluation was consistent with the requirements of

GAMP procedure H64, Section 4.5.4. Specifically, it stated that, The station should

develop a process to evaluate all identified local high points, system high points and

other potential void locations to determine if gas accumulation could occur. It further

stated that. The potential sources of gas intrusion developed as a result of Section 4.1

of this document should be evaluated for applicability to identified high point locations.

Section 4.1 identified a number of gas intrusion mechanisms that included Leakage

form the RCS, Out-gassing of dissolved gas when gas saturated liquid passes from

piping at high pressure into piping at lower pressure, and Leakage through valves,

including leakage through a series of nominally closed valves. Because Section 4.1

of procedure H64 also stated that Potential void locations require further evaluation to

determine what level of monitoring is required, the licensee determined that the safety

injection isolation check valves required verification to ensure their disc were properly

seated following refueling outages to mitigate the possibility for leakage that could

introduce gas into the ECCS piping. As a result, the licensee only verified that these

check valves were seated following refueling outages.

However, during this inspection period, the inspectors noted that this evaluation failed

to consider the possibility of safety injection isolation check valve leakage due to disc

unseating following maintenance outages. As a result, the licensee was not managing

the potential to unseat these valves following maintenance outages which had the

potential to adversely affect gas susceptible locations 1RH-10, 1RH-11, 1RH-12,

1RH-29, 2RH-14, 2RH-17, 1SI-48, 1SI-49, 2SI-40, and 2SI-41 of the RHR and safety

injection systems. In addition, the failure to manage gas accumulation due to potential

safety injection isolation check valve leakage following maintenance outages contributed

to the introduction of a nitrogen void in location 1RH-12 of the Unit 1 B RHR train that

exceed the applicable operability limits. Specifically, this void, which was discovered on

February 10, 2015, was the result of two gas intrusion mechanisms and leakage through

15

the safety injection isolation check valves was one of the associated causes. The

details of this active gas intrusion incident and another licensee deficient performance

associated with this incident are discussed in Section 4OA2.1.c(5) of this IR. The

other cause and associated licensee deficient performance associated with the void

discovered on February 10, 2015, are discussed in Section 4OA2.1.c(3) of this IR.

The licensee captured the inspectors concerns in their CAP as AR01465572. As an

immediate corrective action, the licensee vented the nitrogen that accumulated at

location 1-RH-12. Additionally, the licensee seated the associated check valves,

performed an extent of condition, completed an ACE, and evaluated 1-RH-12 for past

operability. The licensee was in the process of implementing long term corrective

actions that included revising procedures H64 and 1/2C1.2-M4 to verify that the safety

injection check valves are seated as part of the unit startup activities following

maintenance outages.

Analysis: The inspectors determined that the failure to manage potential gas

accumulation due to safety injection check valve leakage following maintenance outages

was contrary to procedure H64 and was a performance deficiency. The performance

deficiency was determined to be more than minor because it was associated with the

Mitigating Systems cornerstone attribute of equipment performance, and affected the

cornerstone objective of ensuring the availability, reliability, and capability of systems

that respond to initiating events to prevent undesirable consequences. Specifically,

the failure to manage active gas intrusion mechanisms at RHR and safety injection

susceptible locations does not ensure the availability of these systems to perform their

mitigating functions. In addition, this failure resulted in the accumulation of gas at the

Unit 1 B train of RHR challenging its operability.

The inspectors determined the finding could be evaluated using the SDP in accordance

with IMC 0609, SDP, Attachment 0609.04, Initial Characterization of Findings.

Because the finding impacted the Mitigating Systems cornerstone, the inspectors

screened the finding through IMC 0609 Appendix A, The SDP for Findings At-Power,

using Exhibit 2, Mitigating Systems Screening Questions. The finding screened as of

very low safety significance (Green) because it did not result in the loss of operability

or functionality of mitigating systems. Specifically, the licensee performed a past

operability review of the void found at 1RH-12 and reasonably concluded that the

system remained operable. The consequence of this void bounded all of the voids

known at the affected locations during this inspection period for the last year.

The inspectors did not identify a cross-cutting aspect associated with this finding

because it was not confirmed to reflect current performance due to the age of the

performance deficiency. Specifically, the GL 2008-01 design reviews were completed

more than 3 years ago.

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires,

in part, that the licensee provide for verifying or checking the adequacy of design, such

as by the performance of design reviews, by the use of alternate or simplified

calculational methods, or by the performance of a suitable testing program.

Contrary to the above, on June 9, 2011, the licensee failed to verify the adequacy of the

RHR and safety injection design. Specifically, the design reviews failed to evaluate the

potential to accumulate nitrogen at multiple RHR and safety injection gas susceptible

16

locations (i.e., 1RH-10, 1RH-11, 1RH-12, 1RH-29, 2RH-14, 2RH-17, 1SI-48, 1SI-49,

2SI-40, and 2SI-41) due to safety injection check valve unseating caused by

maintenance outages.

The licensee is still evaluating its planned corrective actions. However, the inspectors

determined that the continued non-compliance does not present an immediate safety

concern because the licensee vented the nitrogen that accumulated at location 1-RH-12

and seated the associated check valves.

Because this violation was of very low safety significance and was entered into the

licensees CAP as AR 014465572, this violation is being treated as a NCV, consistent

with Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000282/2015008-04;

05000306/2015008-04, Failure to Manage Potential Gas Accumulation Due to Safety

Injection Isolation Check Valve Leakage Following Maintenance Outages)

(5) Failure to Identify a Continuous Gas Intrusion into Residual Heat Removal

Introduction: The inspectors identified a finding of very low safety significance (Green),

and an associated NCV of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective

Action, for the licensees failure to identify a continuous gas intrusion into RHR gas

susceptible location 1-RH-12, which was a CAQ, resulting in a continuous undetected

void growth that exceeded the applicable operability limits. Specifically, the licensee did

not consider applicable active gas intrusion mechanisms when evaluating the discovery

of a void at the RHR piping.

Description: On December 10, 2014, the licensee began a Unit 1 maintenance outage

associated with an RCP seal replacement. As part of the startup activities, the licensee

transitioned to MODE 4 and 3 on December 24 and 25, 2014, respectively. The TS

LCO 3.5.3 required one ECCS train to be operable in MODE 4 when both RCS cold leg

temperatures are greater than the safety injection pump disable temperature specified

in the PTLR. In addition, TS LCO 3.5.2 requires two ECCS trains to be operable in

MODES 1, 2, and 3. The licensee did not verify that the safety injection isolation check

valves were seated as part of the startup activities.

On January 26, 2015, the licensee began a second Unit 1 maintenance outage

associated with another RCP seal replacement. On February 9, 2015, the licensee

transitioned to MODEs 4 and 3. Again, the licensee did not verify that the safety

injection isolation check valves were seated as part of the startup activities.

On February 9, 2015, the licensee also began quarterly gas accumulation inspections

using procedure TP 1468 after transitioning to MODE 3 and were not part of the unit

startup readiness activities following the maintenance outage. On February 10, 2015,

the licensee discovered voids at RHR gas susceptible locations 1RH-12 and 1RH-11.

The 1RH-12 void size was 350 cubic inches, which exceeded the TP 1468 operability

limit of 22.85 cubic inches. The 1RH-11 void size was 62.21 cubic inches, which

exceeded the TP 1468 operability limit of 11.62 cubic inches. The licensee captured the

discovery of these voids in their CAP as AR 01465572 and declared both RHR trains

inoperable while in MODE 1. The licensee declared the system operable later that day

because the void sizes were reduced below their operability limits via venting.

17

However, the inspectors noted that these actions did not consider the known locations

susceptibility to active gas intrusion mechanisms. Specifically, Section 4.9.2 of GAMP

procedure H64 stated that, When an actual gas intrusion event has occurred or there

exists an increased possibility that gas intrusion may occur in a given location or system

the condition should be documented in the corrective action program. It also stated

that, The corrective actions should include additional monitoring. It explained that

Additional monitoring or increased monitoring frequencies should be established when

potential problems are observed, until the root cause of gas accumulation can be

identified and corrected. In addition, it stated that, A monitoring plan with specific

locations, techniques, and frequency should be employed to verify that any gas

accumulation resulting from the active gas intrusion mechanisms remains less than

the volume that challenges the ability of the system to perform its design function(s).

The inspectors were concerned because the affected gas susceptible locations were

vulnerable to active gas intrusion mechanisms and the licensee did not established an

increased monitoring frequency until the root cause of the gas accumulation was found

to verify the sytem remained capable of performing its safety function. Specifically, the

inspectors noted that location 1RH-12 is at the Unit 1 B RHR train downstream of

ECCS injection valve MV-32065 and upstream of the safety injection isolation check

valves SI-9-5 and SI-9-3. Location 1RH-11 is at a similar location at the Unit 1 A train

between MV-32064 and check valves SI-9-6 and SI-9-4. These check valves are in

series and isolate the ECCS from the RCS. In MODE 1, the RCS operates at a

significantly greater pressure and temperature than the ECCS. Thus, leakage of RCS

nitrogen rich water to ECCS may lead to nitrogen out-gassing or steam formation in the

ECCS piping. In addition, the inspectors considered other system interfaces as potential

gas sources.

As a result of the inspectors concerns, the licensee performed an additional inspection

on February 18, 2015. The associated 1RH-11 inspection results did not show evidence

of an active gas intrusion mechanism. However, the inspection discovered a void of

113.8 cubic inches at the 1RH-12 location confirming the existence of a continuous gas

intrusion incident due to an active gas intrusion mechanism. Consequently, the licensee

implemented venting at a periodicity that was based on growth rates. In addition, the

licensee declared the Unit 1 B train inoperable and decided to not declare it operable

until the continuous gas intrusion incident was under control. Following further

prompting from the inspectors, the licensee took chemistry samples of the vented gas

and measured pipe temperatures. The gas was 94 percent nitrogen. In addition, the

1RH-12 piping temperature was warmer than the similar location at the opposite RHR

train and had a temperature profile that was warmer in the vicinity of the check valves.

Thus, the licensee concluded that the check valves were leaking RCS water into location

1RH-12 causing nitrogen to come out of solution due to the lower system pressure.

On February 21, 2015, the licensee vented the piping porting in between the check

valves to properly seat their discs. On February 22, 2015, the licensee declared the

Unit 1 B RHR train operable after confirming that the 1RH-12 void size was below

operability limits and stable.

While the licensee corrected the discovery of a non-conforming void at 1RH-12, which

is a CAQ, on February 10, 2015, the licensee failed to identify the continuous gas

intrusion into this location, which was a second CAQ. The licensee captured the

additional concerns associated with the failed identification of the continuous gas

intrusion into 1RH-12 in their CAP as AR01465572 along with the other concerns

related with the voids discovered on February 10, 2015. These other concerns are

18

discussed in detailed in Sections 4OA2.1.c(3) and 4OA2.1.c(4) of this IR. In addition,

the licensee performed a past operability evaluation and reasonably determined that the

RHR trains remained operable.

Analysis: The inspectors determined that the failure to identify a continuous gas

intrusion into 1-RH-12, a CAQ, was contrary to 10 CFR Part 50, Appendix B,

Criterion XVI, Corrective Action, and was a performance deficiency. The performance

deficiency was determined to be more than minor because it was associated with the

Mitigating Systems cornerstone attribute of equipment performance and affected the

cornerstone objective of ensuring the availability, reliability, and capability of systems

that respond to initiating events to prevent undesirable consequences. Specifically, the

failure to identify a continuous gas intrusion at the Unit 1 B RHR piping resulted in a

void reintroduction of a size that exceeded the applicable operability limits.

The inspectors determined the finding could be evaluated using the SDP in accordance

with IMC 0609, SDP, Attachment 0609.04, Initial Characterization of Findings.

Because the finding impacted the Mitigating Systems cornerstone, the inspectors

screened the finding through IMC 0609 Appendix A, The SDP for Findings At-Power,

using Exhibit 2, Mitigating Systems Screening Questions. The finding screened as

of very low safety significance (Green) because it did not result in the loss of operability

or functionality of mitigating systems. Specifically, the licensee performed a past

operability review of the void found at 1RH-12 and reasonably concluded that the

system remained operable.

The inspectors determined that this finding had a cross-cutting aspect in the area of

human performance because the licensee did not recognize and plan for the possibility

of mistakes when evaluating the gas surveillance results of February 10, 2015.

Specifically, the licensee did not plan for the possibility that the unacceptable results

were indicative of a different problem than originally determined or a combination of

problems. As a result, the licensee failed to identify the continuous gas intrusion

incident. [H.12]

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action,

requires, in part, that CAQs, such as failures, malfunctions, deficiencies, deviations,

defective material and equipment, and non-conformances are promptly identified.

Contrary to the above, from February 10, 2015, to February 21, 2015, the licensee failed

to identify a CAQ. Specifically, the licensee failed to identify a continuous gas intrusion

incident, a CAQ, at RHR gas susceptible location 1RH-12 resulting in a continuous

undetected void growth that exceeded the applicable design limits. The licensee had

sufficient information to identify this CAQ because the GAMP procedure contained

sufficient guidance to determine the source of this void.

The licensee is still evaluating its planned corrective actions. However, the inspectors

determined that the continued non-compliance does not present an immediate safety

concern because the licensee vented the nitrogen that accumulated at location 1RH-12

and seated the associated check valves.

Because this violation was of very low safety significance and was entered into the

licensees CAP as AR 014465572, this violation is being treated as a NCV, consistent

with Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000282/2015008-05;

05000306/2015008-05, Failure to Identify a Continuous Gas Intrusion into RHR)

19

4OA6 Meetings

.1 Exit Meeting Summary

On November 24, 2015, the inspectors presented the inspection results to

Mr. S. Northam, and other members of the licensee staff. The licensee acknowledged

the issues presented. The inspectors asked the licensee whether any materials

examined during the inspection should be considered proprietary. Several documents

reviewed by the inspectors were considered proprietary information and were either

returned to the licensee or handled in accordance with NRC policy on proprietary

information.

4OA7 Licensee-Identified Violations

The following violation of very low significance (Green) was identified by the licensee

and is a violation of NRC requirements, which meet the criteria of the NRC Enforcement

Policy for being dispositioned as an NCV.

that the licensee provide for verifying or checking the adequacy of design, such

as by the performance of design reviews, by the use of alternate or simplified

calculational methods, or by the performance of a suitable testing program.

Contrary to the above, as of November 24, 2015, the licensee failed to verify

the adequacy of the ECCS vent designs. Specifically, the licensee did not verify

that the ECCS vent designs were adequate. As a result, some vents were

inadequate to remove gas that accumulated in excess of the applicable design

limits. The licensee captured their concern in their CAP as AR 01482500 and

AR 01465114, and initiated actions to add and/or modify the vents.

The inspectors determined the finding could be evaluated using the SDP in

accordance with IMC 0609, SDP, Attachment 0609.04, Initial Characterization

of Findings. Because the finding impacted the Mitigating Systems cornerstone,

the inspectors screened the finding through IMC 0609 Appendix A, The SDP for

Findings At-Power, using Exhibit 2, Mitigating Systems Screening Questions.

The finding screened as of very low safety significance (Green) because it did

not result in the loss of operability or functionality of mitigating systems.

Specifically, the licensee evaluated the voids that could not be vented and

reasonably determined they did not result in loss of operability.

ATTACHMENT: SUPPLEMENTAL INFORMATION

20

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

S. Northam, Vice President of Fleet Operations

K. Davison, Site Vice President

E. Blondin, Engineering Director

S. Martin, Performance Assessment Manager

M. Pearson, Regulatory Affairs Manager

J. Connors, Engineering Supervisor

U.S. Nuclear Regulatory Commission

K. Riemer, Chief, Reactor Projects Branch 2

C. Lipa, Chief, Engineering Branch 2

N. Féliz Adorno, Senior Reactor Inspector, Engineering Branch 2

T. Beltz, Project Mananger, Office of Nuclear Reactor Regulation

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Opened and Closed

05000306/2015008-01 VIO Failure to Correct an NCV Associated with Inadequate Gas

Monitoring of Inaccessible RHR Gas Susceptible Locations

(Section 4OA2.1.c(1))05000282/2015008-02; NCV Failure to Manage Gas Accumulation at the RHR Train

05000306/2015008-02 Credited for Emergency Core Cooling in MODE 4

(Section 4OA2.1.c(2))05000282/2015008-03; NCV Failure to Establish Procedures to Verify RHR is Full of Water

05000306/2015008-03 Following Maintenance Outages (Section 4OA2.1.c(3))05000282/2015008-04; NCV Failure to Manage Potential Gas Accumulation Due to SI

05000306/2015008-04 Isolation Check Valve Leakage Following Maintenance

Outages (Section 4OA2.1.c(4))05000282/2015008-05 NCV Failure to Identify a Continuous Gas Intrusion into RHR

05000306/2015008-05 (Section 4OA2.1.c(5))

Discussed

None

Attachemnt

LIST OF DOCUMENTS REVIEWED

The following is a partial list of documents reviewed during the inspection. Inclusion on this list

does not imply that the NRC inspector reviewed the documents in their entirety, but rather that

selected sections or portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

- H64; Gas Accumulation Management Program; Rev. 2B

- H64; Gas Accumulation Management Program; Rev. 2

- TP 1468; Unit 1 GL-08-01 Inspections; Rev. 6

- 1M-RH-TRN A; ECCS Train A: Isolate, Drain, Fill and Vent; Rev. 7

- 1C1.2-M4; Unit 1 Startup to MODE 4; Rev. 2

- 1C1.2-M4; Unit 1 Startup to MODE 4; Rev. 1

- SP 1466; Dynamic Flush of RHR System (GL 2008-01); Rev. 2

- Calc. 32-9236122; Operability Evaluation for Void Found at Location 1RH-11 in the PINGP

Unit 1 RHR System; Rev. 0

- Calc. 32-9237388; U1 RHR System Operability Evaluation for Void 1RH-11; Rev. 0

- Calc. 32-9241892; Operability Evaluation for Void Found at Location 1RH-12 in the PINGP

Unit 1 RHR System; Rev. 0

- NOS Observation Report 2013-03-006; Engineering Programs and Inservice Testing;

dated 09/25/13

- AR01291233; GL 08-01: Void Identified at Susceptible Location 1RH-21; dated 06/20/11

- AR01391787; Misuse of CAP Hinders Fix of GL 08-01 NRC Finding 2011003-09;

dated 07/29/13

- AR01391784; Misuse of CAPAs within the CAP Hinders GL 08-01 Fix; dated 07/29/13

- AR01464866; Void Identified During GL 08-01 Examination; dated 02/04/15

- AR01465572; Voids Identified in RH Piping; dated 02/10/15

- AR01465659; NRC Question: RHR Pump Availability Given Void Inoperability; dated 02/20/15

- AR01466757; Voids Identified in RH Piping at Location 1RH-12; dated 02/18/15

- AR01466999; Void Identified in RH Piping at Location 1RH-12; dated 02/19/15

- AR01467032; Elevated Temperature was Noted on Line 6-SI-25D; dated 02/20/15

- AR01482226; GAMP: Void Identified at Location 2RH-26 and 2RH-09; dated 06/08/15

- AR01482500; GAMP: Void Identified at Location 1RH-04 and 1RH-27; dated 06/10/15

- AR01484195; GAMP: Answer NRC Void Question for 2RH-09 and 2RH-26; dated 06/25/15

- AR01484157; GAMP: Void Identified at Location 2RH-09 and 2RH-26; dated 06/25/15

- AR01488704; GAMP: Acceptable Void Identified During TP 2468 Performance; dated 08/05/15

- AR01466967; Operations Needs to Evaluate Alternate RHR Venting Method; dated 02/19/15

- AR01281658; TI-177 GL08-01 Reviews Did Not Identify Susceptible Locations; dated 04/20/11

- AR01281682; TI-177 - Need Methods to Evaluate Inaccessible Locations; dated 04/20/11

- AR01271826; GL-08-01 TI-177 NRC Inspection Prep - H64 Gap Analysis; dated 02/21/11

- AR01281652; TI177 Results of Susceptible Location Reviews Not Documented; dated 04/20/11

- AR01271024; GL-08-01 TI-177 NRC Inspection Prep - H64 Gap Analysis; dated 02/15/11

- AR01456527; GL-08-01 Inspection Identified Void in Piping; dated 11/18/14

- AR01493599; GAMP: Acceptable Void Identified at 1RH-20; dated 09/17/15

- WO00514236; TP 2468 Unit 2 GL-08-01 Inspections; date 08/27/15

- WO00524641; Perform UT Inspection for GL 08-01 TP 2468; dated 07/09/15

- WO00513378; TP 1468 - Unit 1 GL-08-01 Inspections; dated 02/10/15

2

Corrective Action Documents Generated as a Result of the Inspection

- AR01497409; ECCS Fill and Vent Completed Procedures Not Retained; dated 10/19/15

- AR01498131; Record Pressure/Gas Property for Large Voids Founds; dated 10/22/15

- AR01496469; ACE 01281652 Corrective Actions Were Completed in C Level CAPs;

dated 10/12/15

- AR01497119; Analysis 32-9242120 Missed an Item for Additional Review; dated 10/16/15

- AR01496254; GAMP: H64 Wording Not Clear for Void Checks during Startup; dated 10/09/15

- AR01496191; GAMP: Corrective Action Implementation Was Inconsistent; dated 10/09/15

- AR01495447; GAMP: Vendor Product (EC22242) Does Not List All Susceptible; dated 10/2/15

- AR01495724; GAMP: Typing Error Found in TP 1468; dated 10/05/15

- AR01495444; GAMP: Alternate Testing Method Used but Not Well Documented; dated 10/02/15

- AR01498169; GAMP: Legacy - Ineffective Corrective Action from 2011 CAP 01271826;

dated 10/22/15

3

LIST OF ACRONYMS USED

ACE Apparent Cause Evaluation

ADAMS Agencywide Document Access Management System

AR Action Request

CAP Corrective Action Program

CAQ Condition of Adverse Quality

CE Condition Evaluation

CFR Code of Federal Regulations

CS Containment Spray

DHR Decay Heat Removal

DRP Division of Reactor Projects

ECCS Emergency Core Cooling System

GAMP Gas Accumulation Management Program

GL Generic Letter

IMC Inspection Manual Chapter

IP Inspection Procedure

IR Inspection Report

LCO Limiting Condition for Operation

NCV Non-Cited Violation

NRC U.S. Nuclear Regulatory Commission

PARS Publicly Available Records System

PTLR Pressure and Temperature Limits Report

RCP Reactor Coolant Pump

RCS Reactor Coolant System

RHR Residual Heat Removal

SDP Significance Determination Process

TS Technical Specification

4

K. Davision -2-

If you contest the subject or severity of any NCVs, you should provide a response within 30 days of the

date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,

ATTN: Document Control Desk, Washington, DC 20555-0001, with copies to the Regional Administrator,

Region III; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC

20555-0001; and the NRC Resident Inspector at the Prairie Island Nuclear Generating Plant.

In addition, if you disagree with the cross-cutting aspect assigned to any finding in this report, you should

provide a response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the Regional Administrator, Region III, and the NRC Resident Inspector at Prairie Island

Nuclear Generating Plant.

In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public Inspections,

Exemptions, Requests for Withholding, of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the NRCs

Public Document Room or from the Publicly Available Records (PARS) component of the NRC's

Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible from the

NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Christine A. Lipa, Chief

Engineering Branch 2

Division of Reactor Safety

Docket Nos. 50-282, 50-306

License Nos. DPR-42, DPR-60

Enclosure:

IR 05000282/2015008; 05000306/2015008

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