ML20148R916

From kanterella
Revision as of 04:40, 27 October 2020 by StriderTol (talk | contribs) (StriderTol Bot change)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
Insp Repts 50-327/87-76 & 50-328/87-76 on 871206-880205.Two Violations Noted.Major Areas Inspected:Operational Safety Verification,Maint Observations,Review of Previous Insp Findings,Followup of Events & Review of IE Info Notices
ML20148R916
Person / Time
Site: Sequoyah  Tennessee Valley Authority icon.png
Issue date: 04/08/1988
From: Jenison K, Mccoy F
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II), NRC OFFICE OF SPECIAL PROJECTS
To:
Shared Package
ML20148R847 List:
References
50-327-87-76, 50-328-87-76, IEB-87-002, IEB-87-2, NUDOCS 8804150132
Download: ML20148R916 (71)


See also: IR 05000327/1987076

Text

{{#Wiki_filter:pa Mo UNITED STATES

   p.       og'o,
             ,                      NUCLE AR REGULATORY COMMISSION
                   '
 O"                                               REGloN 11
 $      ,M       .
                                          101 MARIETTA STREET, N.W.
 **            *
                   *                       ATLANTA GEORGI A 30323
  \...../
       Report Nos.:        50-327/87-76, 50-328/87-76
                                                                                                               i
       Licensee:         Tennessee Valley Authority                                                            '
                         500A Chestnut Street
                         Chattanooga, TN 37401
                                                                                                               1
       Docket Nos.:        50-327 and 50-328                License Nos.: DPR-77 and DPR-79
       Facility Name:         Sequoyah Units 1 and 2
       Inspection Conducted: December 6, 1987 thru February 5, 1988
       Inspectors: !_ [ / a M , A                                                     9[S/$'E]
                                                                                     ~0 ate 'Si gned
                       g: M.Jenison.pniopResidentInspector
       Accompanied by:           P. E. Harmon, Resident Inspector
                                 D. P. Loveless, Resident Inspector                                             '
                                 W. K. Poertner, Resident Inspector
                                 W. C. Bearden, Resident Inspector
                                 M. W. Branct), Sequoyah Restart Coordinator
       Approved by-        8
                       4 . R. McCoy, Chief, Projects Section 1
                                                                                          [[h
                                                                                      Efat( Signed
                         Division of TVA Projects
                                                    SUMMARY

l

                                                                                                                '
       Scope:        This routine, announced inspection was conducted on site in the areas
       of:     operational safety verification (including operations performance, system
        lineups, radiation protection, safeguards and housekeeping inspections);
       maintenance observations; review of previous inspection findings; followup of

, events; review of licensee identified items; review of IE Information Notices;

       and review of Inspector Followup Items.
        Results: Two Violations (VIDs) were identified.
                       327,328/87-76-01; Failure to perform adequate post maintenance
                       testing.  (paragraph 9.c)
                       327,328/87-76-02;    Failure to follow procedure,             two examples.
          .            (paragraph 6 and 9.b)
                       One Unresolved Item (URI) was identified during this inspection.
                       URIs are matters about which more information is required to
                       determine whether they are acceptable or may involve violations or
                       deviations.
                       URI 327,328/87-76-03; Fifth vital battery concerns.            (paragraph 3)
   8804150132 800408                                                                                             ,
   PDR      ADOCK 05000327                                                                                       1

! G DCD

                                                                                                      - --
                                                                       _ _ _ _ _ _ -        .    _  _      __.

.

                               2
 Two Inspector Followup Items (IFIs) were identified.
 IFI 327,328/87-76-04; Anubar flow instruments and verification of
 heat exchanger differential pressure. (paragraph 3)
 IFI 327,328/87-76-05; Cable routing deficiencies on Unit 1 cables
 IV1936A and IV1881A.  (paragraph 3)
                                                                   ;
                                                                   I
                                                                     ,
                                                                    1
                                                                    l
                                                                    l
                                                                    l
                                                    _ - _ _
 .
      ,
                                     REPORT DETAILS
   1.   Persons Contacted
        Licensee Employees
        H. L. Abercrombie, Site Director
        J. M. Anthony, Operations Group Supervisor
      *R. H. Buchholz, Sequoyah Site Representative
        M. A. Cooper, Licensing Supervisor
        H. D. Elkins, Instrument Maintenance Group Manager
        R. W. Fortenberry, Technical Support Superintendent
        J. L. Hamilton, Quality Engineering Manager
        M. R. Harding, Licensing Group Manager
      *G. B. Kirk, Compliance Supervisor
        J. T. La Point, Deputy Site Director
        L. E. Martin, Site Quality Manager
        R. W. Olson, Modifications Branch Manager
        B. M. Patterson, Maintenance Superintendent
        R. V. Pierce, Mechanical Maintenance Supervisor
        R. J. Prince, Radiological Control Superintendent
        H. R. Rogers, Plant Operations Review Staff
        M. A. Skarzinski, Electrical Maintenance Supervisor
      *E. K. Sliger, Manager of Projects
      "S. J. Smith, Plant Manager
      *J. H, Sullivan, Regulatory Engineering Supervisor
        B. M. Willis, Operations and Engineering Superintendent
        NRC Employees
      * Attended exit interview                                                      ,
                                                                                     ,
   2.   Exit Interview                                                               l
                                                                                     l
        The inspection scope and findings were summarized on February 5,1988,
        with those persons indicated in paragraph 1. The inspectors described the
        areas inspected and discussed in detail the inspection findings listed
        below.   Dissenting comments were not received from the licensee.        The
        licensee did not identify as proprietary any of the materials provided to

'

        or reviewed by the inspectors during this inspection.
        NOTE:   A list of abbreviations used in this report is contained in          I
        paragraph 19.
        Summary of Violations, Deviations, and Unresolved Items
        (0 pen) Violation (VIO) 327,328/87-76-01; Failure to perform adequate post
        maintenance testing - (paragraph 9.c).

d

        (0 pen) VIO 327,328/87-76-02; Failure to /ollow procedure, 2 examples:       l

, (1) failure to drain a portion of the auxiliary feedwater system in

        accordance with AI-3 in support of maintenance       -
                                                               (paragraph 96); and
                                                                                     i
        __
     .
                                            2
                                                                                       1
       (2) failure to adequately verify hydrogen recombiner orifice clear of
       obstructions per SI-153.4 - (paragraph 6).
       (0 pen) Unresolved Item 327,328/87-76-03; Fif th vital battery concerns -
       (paragraph 3).
       (0 pen) Inspector Followup Item 327,328/87-76-04; Any bar flow instruments
       and verification of heat exchanger differential pressure - (paragraph 3).
       (0 pen) Inspector Followup Item 327.328/87-76-05; Cable routing defi-
       ciencies on Unit 1 cables IV1936A and IV1881A.
  3.   Licensee Action on Previous Enforcement Matters (92702)
       (Closed) VIO 327,328/87-42-01; Failure to Perform 10 CFR 50.59 Safety
       Evaluation for Revision 3 to the FSAR on Hydrogen Analyzer Accuracy.
       Specific corrective action and steps taken to prevent recurrence have been      <
       evaluated and deemed acceptable in NRC Inspection Report 327,328/87-42.
       Additional corrective action by TVA prior to startup was an evaluation of
       past FSAR revisions to verify that proner unreviewed safety question
       determinations (USQDs) had been performed or that no unreviewed safety
       questions existed.      As a result of an NRC review of results of this
       additional TVA evaluation, the NRC requested supplemental information
       concerning the number of additional         safety evaluations that were
       performed. TVA has provided this supplemental information to the NRC in a
       letter (R. Gridley/NRC) dated January 25, 1988.          The NRC inspector

i reviewed this supplemental information and discussed this issue with

       responsible personnel.      TVA's corrective actions appear to be adequate.
       This item is closed.
.       (Closed) VIO 327,328/87-52-01, Example A; Drawings and Instructions Did        ;
l      Not Reflect Skid Mounted Valves and Specified High Point Vent Valves.           l
       This item identified that the design basis for the Essential Raw Cooling

'

                                                                                       !
       Water (ERCW) system was not correctly translated into drawings and              j
        instructions in that skid mounted valves and specified high point vents        i
       were not reflected on the drawings or in the applicable instructions. The        1

2 inspector reviewed the licensee's response to the violation and related  !

        corrective actions.     The inspector verified that the ERCW skid mounted
        valves were added to the applicable system operating instructions and
        surveillance instructions and that the ERCW Centrol Room Drawing was
        red-lined to reflect these valves. The inspector verified that instrument
        high point vents were controlled by SI-604, Essential Instrument
       Operability Verification, for those instruments identified as Unit 2
        restart instruments. The inspector also verified that the commitments           i

, identified in the licensee's response were identified in the licensee's  !

        corporate commitment tracking system. The inspector considers that this
        item has been adequately resolved for restart of Unit 2.
                                                                                        1
        This item is closed.                                                           I
                                                                                       l
                                                                                       I
                                                                                       !
                                                                              _    ._.
                              .                                   --
                                                                           .

'

 .
                                        3
   (Closed) VIO 327,328/87-52-01, Example C; Failure to Assure Applicable
   Regulatory Requirements and the Design Basis are correctly Translated into
   Specifications, Drawings Procedures, and Instructions.            This item
   identified that the four ERCW screen wash pumps were not ASME code stamped
   as required by the design documents.          The inspector reviewed the
   licensee's response to the violation and related corrective actions.        The
   screen wash pumps were designed to ANSI B58.1, were seismically qualified,
   and the motor satisfies class 1E requirements.         As a result of this
   violation the licensee performed a 50.59 evaluation to determine that the
   screen wash pumps are suitable for their application. The licensee also
   committed to revise the FSAR in the next annual FSAR update.             The
   inspector reviewed the 50.59 evaluation and verified that the commitment
   to revise the FSAR was contained in the licensee's Corporate Commitment
   Tracking system.
   This item is closed.
   (Closed) VIO 327,328/87-52-01, Example D; Failure to Transfer the Design
   Basis Into Specifications, in that the metal flexible hose on the ERCW
   inlet to the diesel generator lube oil coolers was purchased to a design
   pressure of 100 psi instead of 150 psi ERCW design pressure.             The
   inspector reviewed the licensee's action to resolve the discrepancy by
   requesting the vendor supply an evaluation that the hose be requalified to
   the 150 psi limit. The vendor, Flexonics Inc, orovided a calculation that
   showed the maximum working pressure for the item was 240 psi and applied a
   conversion factor of 0.97 for the 150'F working temperature.             The
   qualified pressure for the hose at 150 F is 232.8 psi, which is greater
   than hydro pressure of 150% of 150 psi = 225 psi.         The inspector agrees
   that the hose is qualified for the 150 psi application.
   This item is closed.
    (Closed) VIO 327,328/87-52-01 Example E; Failure to Take Adequate Design
   Control Measures, in that the 2A ERCW traveling screen level differential       I
    transformer was disconnectd without proper control and review.           The
    licensee determined that this instrument was inadvertently left off the
   Critical Structures, System and Components (CSSC) list, which resulted in
   work on, and changes to, the instrumentation without implementing the
    controls and reviews associated with CSSC equipment. Temporary Alteration
    Control Form (TACF) 82-258-67 was written to document the present
    configuration of the screen wash level instruments and the disablement of
    the automatic functions they were designed to initiate (i.e., automatic
    backwash of the travelling screens on high differential pressure).        The
    inspector reviewed the TACF and USQD (RIMS #B25 871008 558). This
    evaluation required compensatory measures to manually backwash the screens
    at regular intervals and to dispatch an operator to the ERCW oump house on
    accident conditions to ensure continued ERCW operability. The inspector        l
    reviewed the compensatory measures taken and the procedure changes that        i
    implement those compensatory measures. A Condition Adverse to Quality          l
    Report (CAQR) has been implemented to review the CSSC list against other       l
                                                                                   l
 .
                                       4
   plant documents to ensure that other instruments and components have not
   been left off or removed from the CSSC list.                                          <
   This item is closed.
   (Closed) VIO 327, 328/87-52-01, Example F; Modificetion that Resulted in
   Cross Connecting ERCW Trains. This item ictntified a piping and valve
   assembly that had been installed such that it connected the two drain
   plugs located downstream of valves 2-67-674A ano 674B. The inspector
   reviewed the licensee's response to the J1olacion and gorrective actions.
   The licensee reviewed the DBVP drawing deviations to determine if a
   similar condition existed elsewhere withir thtl w31kd w n r egram. No other
   similar conditions were identified auring thls review.          The licensee
   removed the cross connect piping under work iequest B227E38. The
   inspector verified that the cross cor.. act piping had been removed and
   walked down other safety relatrJ systems to verify thu unauthorized cross
   connects were not installed.
   This item is closed.
   (Closed) VIO 327,328/87-52-02, sxampit A; Failure to Seal Verticai Sleeves            ;
   in the ERCW Pump House As i.eciuired by Drwings. Th? sleeves used to route            1
   instrument sense lines from on' eleyateen to another were found not to be
   packed in accordance C tf1 design drawing reMuirements ts orevent flooding            '
   from one floor to the next. The d i . wings requitGd packicg method: and
                                          .
   materials that were different ;5a6 t@e foend by the inspection team.
   The licensee determ'ined that i onfliccir g ;nd cufusing iastructions on the
   drawings caused the craftsmen to use mater 10h and methods not in
   accordance with the req.frements.        The enti'i EiiLW Jump house was
   inspected by the licensee, and all sleoves were a packed according to
    specifications.   The drawings we chariged to resol,le the conflicting
    instructions.    The in st t :tte reviewed the e spleted aorkplan that
    implemented the sleeve wark (#12f ,' 5) and the OCN ' hat changed the
                                                              ,
   drawings.
   This item is closed.
   (Closed) VIO 327,328/87-52-02 Example B; Heat fracing en ERCW Instrument
    Lines Not Installed as Required by Drawing and Design Criteria.           The
    inspectors found that heat tracing was missing on the RA ERCW pump
   discharge pressure instrument line. Other lu es. coulf net M checked to
    have proper heat tracing due to insulation on the lines.       The liceasee's
    response was to correct the deficiency and to ikmtigate ether lines to
    ensure this heat tracing was correctly instelled. Wort Plan B284704
    re-installed the heat tracing that had been eroved to allcw dccess to a
    spool piece being worked. A walkdown of the CRCW p"mp house an) othet'
    areas exposed to freezing was performed by the licensee in k'P BL.0714 co
    ensure that this was an isolated problem          No other insta7ces veri
    discovered.   The inspectors reviewed the comphted wsrk piar.s to ve-i'y
    corrective actions were complete. In addition, the contraliing procedure,
    Standard Practice (Maintenance)-2, Sequoyah Nuclear Plant Maintenance
                                                                                  ,_ , _
   '
     .
                                              5
       Program, was revised to require CSSC equipment such as the heat tracing
       circuit that was inadvertently left off when WR B123964 was worked on the
       spool piece.                                                                 ,
       This item is closed.
       (Closed) VIO 327,328/87-52-02, Example C; ERCW Flow Transmitter to Station
       Air Compressors Not on CSSC List. The violation is another example of
       instruments required to be on the CSSC list found missing during the
       inspection. In this instance, the instrument was added by an ECN (5414)
       but was not added to the CSSC list due to a lack of awareness by the
       modifications and engineering staff that the instrument was important to
       the reliable operation of safety equipment. The corrective action of the
       licensee was to place the identified item on the CSSC list, and to review
       the CSSC list for accuracy against SMI-0-317-61, which lists those
       instruments required to satisfy surveillance requirements of TS.         To
       preclude further deterioration of the CSSC list, Al-19, part IV has been
       revised to require the CSSC committee to review work plans and ECNs to
       ensure CSSC equipment is properly identified and maintained.           The
       inspector reviewed the corrective actions and determined that they were
       adequate and corrrlete.
       This iten is closed.
       (Closed) VIO 327,328/87-52-02, Example 0, Failure to Establish and
       Implement Written Procedures for Activities Affecting Quality. This item
       identified that the licensee did not have an adequate method for assuring
       that inline instrument and vent valves between the primary root valves and
       the instruments were properly aligned and periodically verified.         The
        inspector reviewed the licensee's response to the violation and related
       corrective actions. 51-604, Essential Instrument Operability Verifica-
       tion, was revised.      An Appendix was added for verification of oroper
       alignment of the inline instrument valves within the Unit 2 DB'IP, phase I,
        system boundaries meeting one of the following: reactor protection set
        inputs, engineered safety feature actuating, Final Ssfety Analysis
       Report, post accident monitoring or Technical Specification devices. The
        inspector reviewed SI-604 for adequacy and verified that the surveillance
        instruction had been revised. The inspector verified the valve alignment
       checklist for numerous safety related in e ruments and verified that the
        long term commitments identified in the licensee's response were ;ontained   1
        in the licensee's corporate commitment tracking system. This item a[ pears   )
        to have been adequa+.ely resolved.                                            I
                                                                                     i

,

        This item is closed.
        (C% sed) VIO 327.328/87-52-02, Example E; Use of Belden Braid Barriers for
        Centrol Pane' Wiring in Lieu of Required Six Inch Separation.     This item
        concerned the design criteria for installation of circuits in panels
        containing both train A and train B class 1E cables. The design
        requirement is six inches of separation or use of a material such as
        Beider Braid. Where Belden Braid is used for redundant class 1E wiring,
                                                                                     l

.

                                                                                      1
                                                                                     I
 .          .

- _ _ _ _ _ - _ _ _ _ . _ _ _ _

                       *
                                 .
                                                                       6
                                   it must be restrained such that the braids do not touch.          Numerous
                                   examples were identified of wiring whose braids were in physical contact
                                   in panel 0-M-27. The violation required corrective action to separate
                                   those identified deficiencies and assurance from TVA that similar
                                   conditions do not exist in other panels.         The cause of the design
                                   deviation was found to be a result of a lack of design detail on the
                                   installation drawings. The use of Belden Braid was determined to be
                                   limited to control room and backup control room boards. Drawings used for
                                   those installations were revised to clearly specify the criteria.       Work
                                   plan 0002-01 was written and imniemented to walk down all panels using
                                   Belden Braid and to correct any inet:llation deficiencies found.         The
                                   field work was completed on January 12, 1988.     The inspector walked down
                                   several panels to determine that the identified deficiencies had been
                                   corrected and to ensure other panels had been checked and corrected by the
                                   work plan.
                                   This item is closed.
                                   (Closed)    VIO 327,328/87-52-02, Example F; Failure to Adequately
                                   Accomplish General Construction Specification G-38 In Routing
                                   Safety-Related Cables. NRC inspection report 327,328/87-52 detailed
                                   findings regarding misrouting of safety related cables IPP718B and IPP712B
                                   which was contrary to the requirements of installation specificatien G-38,
                                   Installing Insulated Cables Rated Up to 15,000 Volts. At the time the
                                   cables were installed, Modification and Alteration Instruction (M & AI)-4,
                                   Installation of Control Power and Signal Cables, contained additional
                                   guidance which allowed routing of cables in short tray lengths near tray
                                   intersections and that the short tray length routes would not appear on
                                   the cable routing cards.       This was allowed if the length of the
                                   unspecified cable was less than 10 feet because some tray designations
                                   change at tray intersections. The TVA response to the violation dateo
                                   November 10, 1987, discussed cable routing including problems and actions
                                   from several programs. These included NRC report 87-18 (Special Test
                                   Inspection), NRC report 87-52 (ERCW As Built Verification), Cable Testing,
                                   Appendix R, and Ampacity programs.     The TVA response dated November 10,
                                   1987, committed to completing the long term cable routing program by
                                   January 1990. NRC review of the TVA response for example F of violation 2
                                   indicated that TVA's conclusion of technical adequacy appeared premature,
                                   since walkdowns and an evaluation of the extent of the problem had not
                                   been completed. Also, additional misroutings of both IE and non-1E cables
                                   identified in NRC inspection report 327,328/87-18 had not been resc1ved.
                                   The review also noted that TVA should address the interaction of free air
                                   space bundling of IE and non-1E       cables together with separation and
                                   segregation criteria in the long range cable routing program and submit a
                                   supplemental response that would include this information. NRC inspectors
                                   reviewed TVA report, "Routing Inconsistencies of Appendix R Cables,
                                   Units 1 and 2, Revision 0" and discussed the basis, methodology, and
                                   results with TVA's Department of Nuclear Engineering personnel.
                                   Two-Hundred/ Seventy-six cabler. required for Appendix R were investigated
                                   by TVA to determine routing. Discrepancies were found between actual
                                   routing and the computer cable routing data base. 'he discrepancies were
                                                                                                                _
  .
,
    .
                                            7                                          -
      evaluated on an individual basis for the attributes of train separation,
      voltage    segregation,   cable ampacity,    tray loading, environmental
      qualification and Appendix R considerations.          The report provided
      justification that the disagreements between actual and design cable
      routing schedules had no safety impact and were technically adequate with        ;
      the exception of two Unit 1 cables which would be addressed by the long
      term cable management program.      The two Unit 1 cables require resolution
      prior to Unit I restart and will be tracked as Inspector Followup Item,
      50-327,328/87-76-05, Cable Routing Deficiencies on cables IV1936A and
      IV1881A.
      Inspectors concluded that the results appeared to be adequate to justify
      the discrepancies and that that Cable Management Program completion date
      of January 1990 is acceptable. The interaction of routed cables in free
      air was inspected and addressed in report 87-65 as Unresolved Item
      327,328/87-18-01.     The supplemental response fcr this violation example
      requested in NRC inspection report 327,328/87-52 for long term resolution
      of free air space issues will be reviewed when submitted. The issue and
commitment will continue to be tracked under TVA's Corporate Commitment
      Tracking System number NCO 870324035. The short term actions and
~
      evaluation are adequate to support Unit 2 heatup and startup.
                                                                                       '
      This item is closed.
       (0 pen) VIO 327,328/87-66-01; Failure to Establish, Implement, and Maintain
       Procedures for System Alignment. The licensee upgraded OSLA 58 to an
       administrative instruction (AI-58) and revised it to correct inadequacies
l      that previously jeopardized system alignment. Inspection 88-06 reviewed

'

<      this procedure and found that revision 1 to AI-58 was adequate to support
       heatup and restart. Performance by the system alignment teams and control
       room operators were also observed in 88-06 and found acceptable to ensure       .
       that the configuration control program will accurately account for              !
       equipment configuration. This violation is no longer considered as a
       heatup item due to the corrective actions that TVA has taken.
l
                                                                                        '
       (0 pen) VIO 327,328/87-66-02; Failure to Establish, Implement, and Maintain
       System Operating Instruction Procedures for System 63 (Safety injection).        1
       The licensee conducted a review of all system operating instruction              l
       checklists comparing them to the actual configuration in the plant and the       l
       system drawings (OSLA-107). Corrections were made to the checkl',sts prior       ,
       to rerunning them to ensure they were adequate.      Some discrepancies were     l
       found in this review during inspection 88-06. This item is considered tied       l
       to violation 88-06-02 since similar findings resulted. A remedial program        l
       to ensure that all hardwart is in the proper position for heatup was
       conducted. The results were reviewed by the NRC and found adequate. This

<

       item is considered adequate for heatup.                                          1
                                                                                        l

. (0 pen) VIO 327,328/88-06-01; Failure to Establish, Maintain, and Implement 4

'
       Procedures for System Alignment. This violation involved failures in
        implementatin of certification requirements, and several isolated examples

I

                                                                      - -           --
              , _   _               _ _ . .          _                    . _ _ _      -. _               __       .. .     .         . _ _ .                . _ _          _           .
                                                                                                                                                                                          ,
                                                                                                                                                                                          t
'                                                                                                                                                                                         '

'.

                                                                                                                                                                                          i
                     '
                                       .

1,

                                                                                                                                                                                          !

'

                                                                                                        .8
                                                                                                                                                                                          i
                                         of failures to maintain configuration control.                                       These items have been
                                         corrected and TVA's corrective actions appear adequate for heatup.                                                                               l
                                                                                                                                                                                          '
i
                                         (0 pen) VIO 327,328/88-06-02; Failure to Establish Adequate System                                                                               ;

4

                                         Operating Instructions. This violation is considered similar to violation

l 87-66-02 in that it represents a failure to correct generic conditions

similar to those of the previous violation. TVA conducted a remedial  ;

1 program to ensure that all hardware is in the proper position for heatup.  ! l Conditions on the checklists that were consid2 red unclear were reverified l 4

                                          and no discrepancies were found. This action is considered adequate for                                                                         ,

,

                                          heatup for both this violation and 87-66-02.                                                                                                    j
'
                                          (0 pen) VIO 327,328/88-06-03; Failure to Prescribe and Conduct Activities                                                                       .
                                          In Accordance With Documented Procedures, Instructions, and Drawings.
                                          This violation relates to conductive material (spare fuses) found in the
                                          diesel generator auxiliary board panel during the NRC walkdown that could                                                                       i

j invalidate seismic qualification of these panels. TVA corrective action l ,

                                          was to walkdown all other seismic panels and to correct any discrepancies.
!
                                          This action ensured that the hardware was adequate for heatup and restart.
                                          TVA also reviewed procedures relating to fuses and found that AI-3 allowed
!                                         fuses removed for clearances to be stored in the bottom of panels. This                                                                          j
'
                                          procedure was changed 4-1 now appears to be adequate. This action is
,                                         considered adequate fot .satup.                                                                                                                  l
(Closed) URI 327,328/86-20-09; Penetration General Design Criteria (GDC)

] This issue involved a question on whether or not the licensee met GDC

1                                         requirements 55 and 56 on specific penetrations for the chemical and                                                                            1

2

                                          volume control system. As a result of the discussions that followed the
                                                                                                                                                                                          '
                                          identification of these specific penetrations, written correspondence
between the licensee and NRC ensued. This written correspondence is

} described in section 3.6 of the Sequoyah SER. As a result the NRC

,                                         determined that the licensee met the GDC in certain cases, in certain

'

                                          cases modifications had to be made to the plant, and finally two
                                          exemptions to the GDC were required. The NRC issued two exemptions to the
                                          applicable GDC requirements (Zech/ White) dated December 3 and 4, 1987,
respectively. This issue has been resolved to the satisfaction of the NRC
as stated in the Sequoyah SER.

i j This issue is closed. I (0 pen) Unresolved Item, 327,328/87-76-03; Fif th Vital Battery and Battery

                                          Room Deficiencies. The safety system outage modification inspection
,                                         (SSOMI) report 86-68 and Inspection Report 87-40 identified several

j deficiencies associated with the fifth vital battery installation.

                                          Pending correction and NRC review of corrective action. TVA has placed a

j caution order on the battery to prevent its use in satisfying Technical

Specification requirements for operation. The caution order does not

{ prevent using the battery for emergencies. This unresolved item is being i opened to track all fifth vital battery concerns that require resolution j prior to accepting the battery for safety related use as a pnwer source to 4

!
1

4 1 1

                                                                                                                                       - - - , - - - - -           ,.n--.~.   , . - - -
  - - . - _ _ .   - ,,. - - . - _ -            . - -
                                                  -
                                                       ,, , _ --,,-.-..,n         - . - - , - - - . - -      _ . .      - ,      a w.                    ~ .
  --   . . - - . - - - - _ -                        - =    -     _     .    .~   - - _ - - -       - - -
     '

l

          -
                                                                                                         t

I 9 I'

l

4

                                                                                                         ;
;

j fulfill Technical Specification roquirements. Items requiring resolution l are: ,

                                                                                                          ,

! a. Seismic qualification documentation for correction of gaps between I

:                            the bottom of the battery racks and the cement pad previously                <
                             identified by NRC report 86-68, deficiency D-2.4-12.                         l

l b. Bend radius violations on battery intercell connectors previously i identified by NRC report 86-68, deficiency D-2.4-13. l

l

J c. HVAC duct installation seismic qualification documentation previously

                             identified by NRC report 86-68, URI U-2.2-1.
~
             d.              Certification for battery rack anchor bolts and battery rack bolts

,

                             previously identified by NRC report 86-68, deficiency D-2.1-7, Sample
                                                                          .
                                                                                                          !
                             45-1, 45-2.

a e. Walkdown inspection observation in 5th battery room identified by IFI

                             87-40-03.
             The items listad above are administrative 1y closed and are now to be
             tracked under one common unresolved item (327,328/87-76-03) in order to                      '

j, ensure comprehensive NRC review. This item is a long term, non-restart '

              item.
             (0 pen) Unresolved Item 327,328/87-18-01, Potential for Secondary Bridging,                  I

d

             Potential Use of Flamemastic as an Alternative to Solid Barriers, and the

i

              Lack of Criteria for Separation of Safety-Related Conduits. NRC special
             test inspection 50-327,328/87-18 documented an example of a train A

, conduit that was routed in close proximity to an uncovered train B cable , I tray. Inspectors expressed concern that a lack of criteria for separation I i of safety-related conduits did not meet the intent of Section 8.3 of the l j '

              FSAR in that protection and indepenuance of redundant circuits may be                        I
              compromised. This item also included concerns regarding routing of cables
              in free air and examples of cables which had been mis-routed in
j             unspecified trays. The status of these items was reported in NRC inspec-

<

'
              tion report 327,328/87-65, which had three remaining items requiring
              further review after additional licensee action.                  NRC report 87-65

1 reported correction of 2 non-divisional cables that had been misrouted in I a divisional tray. The three remaining items included: (1) correction of

a divisional cable that had been misrouted in a non-divisional tray;
'
              (2) the potential for secondary bridging due to misrouting of cables in

l cable trays; and (3) both an example and the generic concern regarding the

,             lack of criteria at Sequoyah for separation between cable trays, and
I             conduit runs. Section 8.3 of the Sequoyah FSAR includes requirements for
:             separation of cable trays, however, it does not address a criteria for
i             conduit / conduit or conduit / tray separation. A review of TVA construction
i              specifications, modification procedures, and conduit installation proce-

1 dures in conjunction with TVA/NRC discussiens indicated a lack of guidance

]              in this area.              NRC letter S. D. Richardson /NRC to S. A. White /TVA of
1
,
              December 31, 1987, "Criteria For Separation of Safety-Related Conduits

.

                                     10
 (NRC Inspection Report 327,328/87-18)", was sent to TVA after a technical
 review raised significant questions as to the adequacy of installations at
 TVA. The letter requested TVA provide analyses to demonstrate that faults
 in one raceway (conduit or cable tray) would not cause internally
 generated fires that affect the functional integrity of redundant safety-
 related circuits in adjacent raceways.       The letter required a response
 within 30 days and resolution of the concern prior to the restart of the
 Sequoyah units.     CAQR SQN871585 was written to address item #1, the
 divisional cable that was misrouted in the non-divisional cable tray. NRC
 inspectors reviewed the CAQR and performed a field inspection to verify
 the cable had been restored to the correct divisional tray.        Item #1 is
 closed.    Item  2 regarding  the potential for secondary  bridging  due to
 misrouting of cables in cables trays, is addressed in NRC Inspection
 Report 327,328/87-52.     Item #2 is closed.     Item #3, the example and
 generic concern regarding the lack of criteria for conduit / cable tray
 separation, has been reviewed. The specific example in NRC Inspection
 Report 327,328/87-18 envolved a 3-inch train A conduit (2M-3240-A) which
 was routed across the top of a train 8 cable tray (MS-B). Inspectors
 reviewed cable and conduit records for conduit 2M-3240-A and cable tray
 MS-B at the interaction point. Records indicated that the tray contained
 several Unit 1 cables and 4 low voltage Unit 2 conductors associated with
 the spent fuel pit pump B-B, spent fuel pit heat exchanger A & B and CCS
 booster pump 2B-B. The interacting conduit contained 5 low voltage
 Unit 2 cables for the pass system.       Inspectors concluded that as both
 interacting raceways contained low voltage cables and there was some
 separation between the cable tray and conduit, rasoluti.,n of this specific    ,
                                            Inspectors discussed the generic
                                                                                '
 example is not required for heatup.
 issue with TVA and t.icensing personnel. The TVA formal response to the        !
 NRC letter had not been drafted. This item is open pending NRC review of
 TVA's formal response.     This is a startup item.
 (Closed) Unresolved Item 327,328/86-68, U-2.4-3, Unknown effect on bearing
 pressure on Class 1E cables in unsupported vertical bundles. Unresolved
 Item U-2.4-3 was opened in NRC Inspection Report 327,328/86-68 due to
 field inspection in the cable spreading room which resulted in a concern
 that vertical bundles of flamemastic coated IE and non-1E cables had
 excessive bearing pressure where the bundle drops over the sharp edge of a     !
 cable tray. The NRC inspectors discussed the issue with TVA's Department       i
 of Nuclear Engineering personnel and viewed the Wyle video tapes of tests
 run to determine adequacy of the static and dynamic loading on the cables
 due to weight of the cabling and the weight of the flameastic that was
 added after construction. Inspectors also reviewed test results used        to
 justify ampacity reduction values used by TVA.          TVA staff and Wyle
 personnel concluded that bearing pressure was not adequately addressed for
 vertical bundles that drop over sharp edges. This was addressed during         )
 the exit and the Site Director committed to addressing the issue prior to      l
 unit    restart.    NRC  inspectors reviewed a memorandum (J. Hosmer,          i
  TVA/M Harding, TVA, Sequoyah Nuclear Plant        -
                                                       Resolution of Bearing
 Pressure on Air Drop of IE Cables - NRC commitment No. NC087-0029001)
 which contained summary justification for the issue being a non-restart        i'
  item.   The memorandum transmitted DNE calculation SQN-E2-031 (RIM B25
                                                                                 I
                                                                                 l

.

                                    11
 880108 815, Sidewall Bearing Pressure For Class 1E Free Air Drops) and
 NUREG/CR-4548 (Correlation of Electrical Reactor Cable Failure With
 Materials Degradation, March 1986). Inspectors reviewed the references
 and discussed the issue with DNE engineers that performed the calculation.
 The DNE calculation indicates that several cables within the bundle have
 bend radius violations and that the cables exceed the allowed bearing
 pressure calculations by a factor of 5 to 6. Cable loading ~ due to weight
 was well within calculated limits. Due to the complexity of the issue,
                                                               .
 the potential long term corrective action, and existance of a long term
 post-restart Employee Concern (CATD) No.109.00-NPS-01 R3 concerning bend
 radius violations, a brief summary is presented below to facilitate future
 inspection efforts.
 The TVA DNE calcu14 tion selected a worst case bundle based on a walkdown
 of the cable spreading room. Although cables 1n the worst case bundle
 exceeded bearing pressure limits, NRC inspectors concluded that the issue  ,
 did not meet the accepted TVA Sequoyah restart criteria based on the       i
 following information: (1) conservative assumptions were made that the     !
 entire weight of all cables and all flamemastic was bearing on the sharp   !
 edge; (2) the calculation assumed cables with the lowest bearing pressure
 limit were the cables in contact with the sharp edge; (3) no credit was    ,
 taken for support offered by the rigid flamemastic; (4) the weight of      i
 flamemastic was calculated using the          length of run, times the
 cross-sectional area difference between the sum of the area of a circle    l
 that would encompass the bundle and the cable cross sectional area of the  !
 cables; (5) no credit was taken for bottom support where cables entered    :
 other trays; and (6) no credit was taken for increased surface area        ;
 (increased support) due to flamemastic on-each side of the cables at the   l
 point of contact with the sharp edge.           Inspectors concluded that  !
 quantitative inclusion of all conservatisms may have reduced the bearing   ;
 pressure to an cceptable value, however, bend radius violations would      l
 still exist.    Testing information prepared by Sandia National Laboratory l
 and included in NUREG/CR-4548, Correlation of Electrical Reactor Cable     '
 Failure With Materials Degration, indicated that "creep short out" due to   I
 applied stress on a cable over a radius causes a slow migration of the     '
                                                                             '
 conductor through the insulation. The phenomena is temperature dependent
 with a slow relatively linear creep rate at room temperatures and shows    f
  little change between 1 day and 40 years. Several mitigating f actors      '
 would tend to minimize the effect with time.        These factors include:  1
                                                                             I
 (1) as the applied stress tends to flatten the conductor strands, the
  surface area in the direction of the stress increases which in turn
 decreases the cross-sectional force reducing the creep rate; (2) as the
  ir,sulation deforms, it widens and provides a greater area to support the
 given stress; (3) as the insulation and conductor conform to the radius at
 the point of contact the applied stress seeks uniform distribution over
 the entire contact area; and (4) insulation aging and irradiation (where
 applicable) tend to harden polymer and rubber insulation reducing the
 creep rate. Cracking as related to bearing pressure is not of significant
 concern as it is mainly related to tensile stresses rather than the
 compressive stresses associated with creep short out. Hot cracking of
  stressed bends in cables does occur but is associated with multiple
                                                                            !
                                                                            !

.

                                     12
 thermal cycling of the cables above 175 degrees F. Inspectors concluded
 that the conservatism in the calculation and the mitigating factors offer
 reasonable assurance that the installation is satisfactory for heatup,
 startup and operation. Further evaluation and possible long term
 corrective action is necessary as testing data with regard to age (i.e,
 justification for use as a basis for a 40 year qualified life) contains
 unverified extrapolations from limit test data in an area that is not well
 understood. This item is closed and will be continued to be reviewed as
 Sequoyah Employee Concern Corrective Action Tracking Document (CATD) No.
 109.00-NPS-01 R3 and Corporate Committment Tracking System item
 NCOS7-0029001 as a post restart item.
 (Closed) Violation 327,328/86-68-02, paragraph c, section 2.1.3.1,
 inspection sample number 1-2; Lack of Material Certification for 1-1/8"
 Diameter Studs and Nuts for Auxiliary Feedwater Pump 2A-A Discharge Flange
 to Navco Spool Piece 2AFO-13. During the NRC Safety System Outage
 Modification Inspection (SSOMI) 327,328/86-68, material certification
 could not be located for the 1-1/8" diameter studs for Auxiliary Feedwater
 Pump 2A-A discharge flange.       Subsequent investigation by TVA failed to
  locate the missing certification. Lacking documentation of certification
  required removing paint from the studs in order to inspect vendor markings
 and certify the material. Work request B244476 was completed on January
  19, 1988, and documented removal of paint and certified vendor markings on
 the studs in question.    Inspectors reviewed the work request against the
 original specification for the studs and then conducted a field inspection
 of the studs. The studs were found to be ASTM A 193, Grade 87 as required
 by the material specification.     Licensee action on this item is adequate.
  This item is closed.
  (Closed) VIO 327,328/84-11-02; Failure to Use Appropriate Orawings During
 Maintenance.    This violation involved maintenance personnel rewi*ing a
  PORV controller they interpreted as being incorrectly wired by reviewing a
  single drawing. The cause of the violation was determined to be personnel
  error in failing to obtain and review all applicable drawings. Further
  review by the licensee has determined that the single drawing reviewed
  could have been adequate, and that the error made was in the review
  process. Further review of additional drawings might have prevented the
  error, but there is no conclusive evidence that the same error woulu not
  have been made regardless of t t.e number of drawings reviewed.         The i
  misinterpretation of how the PORV's bistable pressure switches actually
  functioned was an avoidable mistake, but might have been made in spite of
  a more extensive review, because the other drawings would have shown the    ,
                                                                              ~
  same switch arrangement. The misinterpretation of the circuitry involved
  is considered an isolated event. The individuals involved were counselled
  and training was ccnducted to remind instrument maintenance personnel to
  obtain and review all applicable drawings during maintenance and
  modifications planning.    This corrective action is considered adequate.
  This item is closed.                                                         '
                                                                             _

.

                                      13
 (Closed) VIO 327/84-24-03; Inadequate Tool Control. This flux thimble
 guide tube ejection event item was reopened in Inspection Report 327,
 328/87-43 when all the items associated with this event were reopened for
 further review for adequate corrective actions. After reviewing the root
 cause determination and the corrective actions, the inspector determined
 that this item was adequately identified and corrected. Said review was
 documented in Inspection Report 327,328/87-50.
 This item is closed.
 (Closed) VIO 327,328/86-68-01; Failure to Assure that Applicable ASME Code    :
 Requirements Were Included in the Procurement of Specific Safety-related
 Code Class Equipment. This violation had three examples as addressed in       !
 the notice of violation dated April 24, 1987. Example A was closed in
 Inspection Report 87-60. Examples B and C were closed in Inspection
 Report 87-40. Therefore, violation 327,328/86-68-01 has been addressed in
 its entirety.
 This item is closed.                                                          ,
                                                                               i
 (Closed) VIO 327,328/86-68-03; Failure to Identify and Control Materials,     ;
 Parts, and Ccmponents by Heat Number, Post Number, Serial Number, or Other    !
                                                                               '
 Appropriate Means. This violation contained three examples including
 multiple deficiencies as addressed in the notice of violation dated April
 24, 1987. All deficiencies were addressed with adequate results in
  Inspection Report 87-40. Therefore, violation 327,328/86-68-03 has been
 addressed in its entirety.
 This item is closed.
                                                                               ,
 (Closed) URI 327,328/87-52-05; Concern Over Obsened Flow Conditions For
 Diesel Generator Coolers and Upper Containment Coolers. This item
 concerned the adequacy of the installed flow instruments and configuration      ,
 control and equipment degradation aspects of the inspectors' observations.      '
 The inspector reviewed the closure package associated with this item and      ;
 determined that the flow to the coolers was being controlled in that the
 configuration log reflected that flow was established. With respect to
 the adequacy of the installed gages the licensee determined that the gages      i
 are designed for an overranging application and that the gages are used         j
  for local indication only. The licensee is reviewing the system design to
 determine if larger scale gages would be more appropriate in these
  applications.
 This item is closed.
  (0 pen) VIO 327,328/87-60-02; Failure to Meet The Requirements of 10 CFR
  50.59. This violation resulted from the licensee modifying the AFW system
  such that the 2A-A AFW pump could no longer deliver 440 gpm as required by      I
  the TS. This violation is presently under consideration for escalated
  enforcement. The licensee has replaced the pump internals on the 2A-A AFW
  pump to ensure that the pump will be able to deliver the required flow to
                                                                                1
                                                                                 !
                                                                                    .
   '
     .
                                                                                    i
                                           14
       the steam generators. The inspector witnessed initial testing of the 2A-A
                                                                                    '
       APd pump af ter maintenance was completed and verified that the pump could   ,
       deliver greater than 440 gpm. The licensee's actions have resolved the
       inspector's concern with TS compliance and are adequate for the restart of
       the Units. This item will remain open pending enforcement action.
       (Closed) URI 327,328/87-54-01; Implementation of Commitments. This item

l identified that the Corporate Commitment Tracking system was not effective

       in ensuring thot commitments were met. The inspector conducted interviews

a

       with appropriate licensee personnel and verified that selected open

i commitments were being tracked by the licensee. Since this item was

       opened there have been numerous instances where the licensee has notified
       the NRC verbally, on the day that a commitment was due, that the
       commitment due date would not be met. The concern over missed commitment
i
       due dates was discussed with the plant manager at the exit interview. The
       problem appears to be a notification problem and not a commitment
       completion problem. No commitments were identified by the NRC inspector
       which did not appear in the CCTS and were being tracked by the licensee.
       The licensee is aware of the commitments and when they are due; however,
       the licensee has not instituted an effective method of ensuring that the
       due dates are met or that the NRC is notified prior to the commitment due
l      date being missed. Although no regulatory requirements were violated,
i      the inspector will review this area during routine monthly inspections

I '

       to determine if the licensee has made progress in resolving missed           e
       commitment due dates.
       This item is closed.
       (Closed) URI 327, 328/85-16-03; Seismic Design of Vital Batteries Con-

'

       cerning Use of Spacers At End Rack. This issue involved the adequacy of
        the seismic installation of the plant vital batteries.       The inspector

! reviewed TVA and vendor installation drawings against the field

l      configuration of the battery racks for the 125V vital DC battery banks and
        the diesel generator battery banks. The 125V vital DC battery racks were
        installed in accordance with applicable vendor drawings; however, TVA had
        received a memorandum dated, March 27, 1985, from the vendor, GNB
       Batteries, Inc., stating that there may be a gap between the end cell and     ,
        end stringer of greater than 1/4-inch in some Class IE battery               ;

}. installations. A gap greater than 1/4-inch was determined by the vendor i )~

        to be unacceptable. This recommendation was apparently based on the          !
        configuration used for seismic qualification testing of the batteries. A

i review of the installation indicated that gaps of approximately 1/2-inch

        existed at one end of some of the racks. The vendor drawing did not show
        a gap limit or a spacer        or the original installation.   The vendor
        recommended that a spacer be inserted to bring this gap to less than 3/8-

1 inch. TVA has initiated workplans to install spacers of an approved

 i      material in the vital battery banks. The inspector requested tha'        .e
        licensee provide further information concerning TVA's actions in re ,onse
,       to the vendor notice, including any determination concerning operability

j during a seismic event. The site Office of Engineering (OE) field

        inspected the vital batteries on April 19 and 20,1985, and determined
        that the vital batteries had end ,aps greater than recommended by the
                                                                                :
                                                                                ;
 .
                                                                                ,
                                       15
   vendor. A Nonconformance Report (NCR) was written by site OE dated           .
                                                                                '
   April 24, 1985. The NCR states, "The spacing between the end cell and end
   stringer of the rack on vital batteries I thru IV was measured and found     l
   to exceed 1/4-inch required by seismic testing. The fifth vital battery
   has one cell missing at the present time and no spacer was added." The       ;
   NCR further states the following:                                            t
         "In the absence of spacers, seismic loading could cause failure of
         the vital battery cells.    There is eviderce that structural failure
         would likely occur at the battery terminal posts. Such a failure of    +
         one cell causes the loss of the entire battery system. Although it
         was not possible to analytically predict the seismic behavior of
         unqualified (without spacers) configurations, a failure of this type   '
         must be considered probable."
   The condition was defined as a "significant condition adverse to quality."   i
   The NCR was signed by the responsible Branch Chief on April 24, 1985.        .
   This date was corrected on a later copy to May 1, 1985, due to changes       t
   after an additional OE review. The NCR was received by the site Office of    !
   Nuclear power (NUCPR) on May 1,1985. In memoranda dated May 29 and           ,
   June 5, 1985, NUCPR rejected the NCR and subsequent Failure                  !
   Evaluation / Engineering Report (FE/ER). The memoranda stated that, "This    i
   item was handled by Sequoyah Site Services under the operating experience    !
   review program. In addition, this item was not an OE nonconformance nor a     ,
   breakdown in an OE QA program requirement; therefore, it should not have     !
   been written. This item required expeditious maintenance activities and      ,
   was acted upon by the plant staff when a copy of the vendor letter was       i
   received." The inspector reviewed the PRO (1-85-100) written on this         '
   event to document the plant staff review.        The documents stated the
    following conclusions:
                                                                                  I
   -
         An evaluation of the vendor letter by plant Compliance personnel
          determined that the recommendation had no effect on . battery
          operability; however, personnel did consider the recommendation to be
          a prudent maintenance practice.
   -
          Compliance personnel determined the absence of between-cell spacers
          did not adversely effect operability of the batteries.
    -     Because the recommendation was associated with seismic testing, it
          was handled on a priority maintenance bas's; however, inspection of
          the physical mounting of the batteries and discussions of the
          manufacturer's recommendations led to the :onclusion that it was not
          a condition of operability.
    These statements are in direct contradiction to the NCR written by the
   Office of Engineering, yet no coordination of these conclusions is
    apparent between OE and Plant Compliance.
    10 CFR 50, Appendix A, Criterion 2, Design Bases for Protection Against       i
    Natural Phenomena, states: "Structures, systems, and components important     l
                                                    _ _ _ _ _ _ _ _
                                                                    .
                                                                          ..

'

 .
                                       16
   to safety shall be designed to withstand the effects of natural phenomena
     uch as earthquakes, tornadoes, hurricanes, floods, tsunami, and serches
  without loss of capability to perform their safety functions. The design
  bases for these structures, systems, and compenents shall reflect:
   (1) Appropriate consideration of the most severe of the natural phenomena
   that have been historically reported for the site and surrounding area,
  with sufficient margin for the limited accuracy, quantity, and period of
   time in which the historical data have been accumulated, (2) appropriate
   combinations of the effects of normal and accident conditions with the
   effects of the natural phenomena and (3) the importance of the safety
   functions to be performed."
   Regulatory Guide 1.10, Seismic Qualification of Electric Equipment for
  Nuclear Power Plants endorses IEEE standard 344-1975, recommended prac-
   tices for seismic qualification of class 1E equipment for Nuclear Power
   generating stations, which states that:
         "The seismic qualification of Class 1E equipment should demonstrate
         an equipment's ability to perform its required function during and
         after the time it is subjected to the forces resulting from one SSE.
         In addition, the equipment must withstand the effects of a number of
         OBEs (see Sections 5,4 and 6.1.4) prior to the application of an SSE.
         The equipment to be tested shall be mounted on the vibration
         generator in a manner that simulates the intended service mounting.
         The mounting method shall be the same as that recommended for actual
         service. The mounting method shall use the recommended bolt size and
         configuration, weld pattern and type, etc. The effect of electrical
         connections, conduit, and sensing lines, etc shall be considered.
         The orientation of the equipment during the test shall be documented
         and shall be the only orientation for which the equipment is
         considered qualified unless adequate justification can be made to
         extend the qualification to an untested orientation."
  TS 3.8.2.3 requires that the following D.C. vital battery channels be
   energized and OPERABLE:
  CHANNEL I       Consisting of 125 volt D.C. board No. I, 125-volt D.C.
                  battery bank No. I and a full capacity charger.
  CHANNEL II      Consisting of 125-volt D.C. board No. II, 125-volt D.C.
                  battery bank No. II, and a full capacity charger.
  CHANNEL III Consisting of 125-volt D.C. board No. III, 125-volt D.C.
                  battery bank No. III, and a full capacity charger
  CHANNEL IV      Consisting of 125-volt D.C. board No. IV, 125-volt D.C.
                  battery bank ND. IV, and a full capacity charger.
  Contrary to the above, on April 2, .986, TVA engineering received a letter
   from GNB Batteries, Inc. stating that the installed 125V vital batteries
  did not meet the tested configuration. Plant personnel received this
                                                                                   .
  -                                                                                r
    .
                                             17
      letter on May 1, 1985. Adequate justification was not made to extend the
      qualification to the untested configuration. Installation of battery end
      spacers to correct this problem was accomplished on May 14, 1987.     During
      this time period, Unit 2 was operated without declaring the vital
      batteries inoperable, or meeting the required action statement.          In
      accordance with the "General Statement of Policy and Procedure for NRC
      Enforcement Action," 10 CFR Part 2. Discretionary Enforcement, the event
      described above meets the following criteria:
      -      The Licensee was forced into an extended shutdown related to poor
             performance over a long period following their August 1985 shutdown.
                                                                                   '
      -
             The Licensee has developed and is aggressively implementing their
             Nuclear Performance Program for problem identification and
             correction.
      -
             NRC concurrence is needed by the Licensee prior to restart.
      -
             Enforcement action is not necessary to achieve remedial action.
      -
             The violation occurred prior to the August 1985 shutdown.
      -
             The violation was non-willful and would not have been categorized as
             higher than Severity Level III under the NRC's enforcement policy.
      The inspector reviewed the memorandum from GNB batteries, Inc. to TVA
      dated March 27, 1985. It contains information as discussed above which
      appears to be reportable under 10 CFR Part 21. This issue is being           .
       reviewed by OSP staff and will be discussed with the vendor. The current

,

      configuration of the vital batteries includes end spacers as recommended
'
       by the vendor.      This was verified by a walkdown conducted by the
       inspector,

i This item is closed.

       (Closed) URI 327,328/87-17-01; Loss of ERCW Caused Inoperability of         r
       Control Room Ventilation, Radiation Monitors and the Operating Train of      i

4 RHR. This URI addressed an event which occurred March 11, 1987. An ASE  !

i      shut valve 1-FCV-67-127 in a hold order for work to be performed on the
i      ERCW piping.     This rendered the A train equipment inoperable.       The   l

I

'
       operator failed to realize that 0-FCV-67-208 was shut making inoperable a
       portion of the B train supplying the station air compressors.
       Approximately three hours later it was discovered that the station air
       compressors had tripped on lack of cooling water. This tesulted in a loss
       of control air to valves in both trains of control room ventilation and
        isolated four radiation monitors.        This event occurred because the
       operator failed to verify that all of the B train ERCW was operable before
        isolating the A train. In addition, the 1A RHR pump room temperature was
       noted to be increasing following the event. This was caused by continued
       operation of the 1A RHR pump following room cooler isolation.                l
   .   . . _ -                                       --                  -
                                                                                                                                                 I,
     -
            .
                                                  18

,

              The inspector considered the following in review of this event:
              -
                   Appropriate use of procedures

3

               -
                   Independent verification of actions affecting quality                                                                        !
-
                   Configuration control throughout the event                                                                                     !
              -
                   Corrective actions taken following initial discovery of the problem                                                           l
                                                                                                                                                 t
                                                                                                                                                 '
                   Appropriate Use of Procedures / Control of Plant Configuration
                   During the midnight shif t on March 11, 1987, an SRO received a
                   clearance request to tag the A train ERCW discharge header in order
                   to replace the 24-inch piping from 2-FCV-67-146 to the first                                                                  )

4 discharge header tee. This work was to be performed per WP12313

                   under WR B202762. In an interview, the SR0 stated that he began                                                                '

i preparing the clearance, but had not fully completed the review by ] the end of his shift. The oncoming SRO took the clearance and with

'
                   minimum review (which was normal procedure at the time) proceeded to
                   hang the hold order tags and isolate the header. The clearance did
                   not state that this action would make the operating train of RHR
                   inoperable by isolating the associated room cooler. Interviews with                                                           l
                   the preparer of the clearance revealed that he had assumed that
                   compensatory measures would be taken at the time the tagging was
                   accomplished in order to keep the operating train of RnR operable.                                                           l'
                   The SRO tagging the system stated that he failed to realize the
.
f
                   error.
                   TS 3.4.1.4 states that, "Two residual heat removal (RHR) loops shall
                   be OPERABLE and at least one RHR loop shall be in operation." The                                                             >
l                  action statement requires that, "With less than the above required
                   RHR/ reactor coolant loops OPERABLE immediately initiate corrective
                   action to return the required RHR/ reactor coolant loops to OPERABLE                                                           i
                    status as soon as possible."

1 Contrary to the above, on March 11, 1987, the licensee made j inoperable the operating loop of RHR and did'not realize or correct ,

                   the condition for 10 hours. The pump, however, did continue to                                                                 <
                   operate during this time. This is an example of violation 87-30-01
,                  which was discussed with Mr. S. A. White in a letter dated July 20,
                    1987.    This multiple example violation involved procedural
!                   inadequacies and/or inadequate procedure implementation which has                                                              i

j given cause for concern over the control TVA's staff has over

'
 i                  Sequoyah's operational activities, particularly in the areas of
                    system and equipment status, procedural changes and testing,                                                                  j
 .
                   Corrective actions currently in progress for violation 87-30-01                                                                 '
 I                  should correct the problems that caused chis event.                                                          Therefore, TVA
)                   need not respond additionally to this example of the violation.
1                   The SRO who tagged out ERCW A train equipment also did not realize
.                   that the B train supply to the station air compressors through valve

l 0-FCV-67-208 was also isolated. 0-FCV-67-208 was not on 501-67.1,

!                   Essential Raw Cooling Water System, that was current's on record.

I

                                                          . ____ _ _ __ ________ __ _ ._______________ _______ _ _ ___________ -
        .        .     .
    *
          .
                                                                                          '

1'

                                               19
i
                 Therefore the ASE had no indication that the valve was closed. TVA       '

i had already identified this error and had corrected 501-67.1 in

                 revision 27 dated November 14, 1986.      The licensee f ailed to re-run 1
!                the procedure or verify the correct position of 0-FCV-67-208             l
                 following the update.
                                                                                          !
                 TS 6.8.1 requires that written procedures be established, implemented
                 and maintained covering the referenced activities. Contrary to this,
!                SOI-67.1 failed to verify the correct position of 0-FCV-67-208 and

I avoid making required safety-related equipment inoperable. This

                  situation existed over four months following the discovery of an
error in the procedure.
                 This violation is considered a further example of 87-30-01 and
                 corrective actions in progress should prohibit repeat occurrences of
                  this event. Therefore, TVA need not respond to this example of the
j                 violation.
                   Independent Verification of Actions Affecting Quality
                  The inspector determined that independent verification was lacking in
                  the preparation of the hold order (number 2262). This problem smong
                  others with the c'earance program at Sequoyah is being corrected
                   through corrective actions being performed under violation 87-30-01.
                  The inspector determined that the laydown and isolation of the hold
                  order boundary was independently verified and did not contribute to
                   this event.                                                             <
I
~
                  Corrective Actions Taken Following Initial Discovery of the problem
 l                 Following the initial loss of service air the SRO re-reviewed the
                   clearance and began walking down the hold order boundary.        This
                   review found and corrected the problem with the service air
1                  compressors. It failed, however, to discover the problem with the
                   operating train of RHR. Additionally, the inspector found the unit
                   operators response to the event to be inadequate in that the root
j                  cause for the problems was never determined.      Corrective actions
  ;                currently in progress for violation 87-30-01 should correct the         i
                   problems that caused this event. Therefore, TVA need not respond
                   additionally to this example of the violation.
I     The inspector had no further questiot       .   cerning this event.  This item is     l
i     closed.                                                                              '
i
~
            (Closed) VIO 327, 328/86-68-05, paragraph c, section 2.5.5, deficiency
            0-2.5-1; Auxiliary Control Room Indicator Modules Power Separation and
  ;         Mounting.     This issue involved an observation that Module side panel
            protectors were missing on indicators for safety train A and B. Modules         >
            had engaging latches loose or not engaged, compromising seismic mounting.       l
                                                                          The inspector
'
            Additionally, one cable had four bare exposed leads.
j           reinspected panels in the auxiliary control room and determined that all
j           deficiencies previously noted had been corrected.
 l
            This item is closed.
                                                                                            l
                                                    _
                                                                                _
                                                                                        -

.

                                     20
 (Closed) URI 327, 328/87-02-05; Adherence to Directions from HP Techni-
 cians and Compliance with HP Practices. During a tour of the auxiliary       .
                                                                              '
 building, an NRC inspector noted that a worker had violated a "notify HP
 prior to entry barrier" and had entered to perform a task contrary to
 instructions given to the worker to remain outside the area until the
 smear in the area had been counted.      The HP technician had frisked the
 area in addition to taking a smear.      The entry took place while the HP
 technician had lef t to count the smear sample. The smear sample results
 showed no contamination.     The NRC inspector interviewed all workers in
 the area, as well as the HP technician, and cautioned them on compliance
 with HP procedures including verbal instructions. The NRC inspector
 discussed the matter with the HP superintendent and the modifications        ,
 supervisor and noted that increased emphasis would be placed on monitoring   ;
 HP practices during inspectors' tours. Due to the low safety e ,nificance    ,
 of this particular incident, it was characterized as unresolved pending
 future observation of routine HP practices. 7he inspection staf f has
 noted few discrepancies in this area since the January 1987 instance. In
 addition, all 1987 raciological incident reports to date have been
 reviewed for recurrence of incidents of this type.      No similar instances
 were noted. It was noted, however, tho. second offenses for infractions
 such as wearing the wrong TLD have resulted in three day suspensions and
 two cases of entry into a iiigh radiation area with improper dosimetry have
 resulted in employee ttrmination.
 This item is closed.
 (Closed) URI 327,3;J/87-50-03; Containment Spray Pumps.         This issue
  involves a lack of retrievable documentation to substantiate discisions     i
 made to install an orifice in the Containment Spray (CS) system.         The :
  licensee committed to the following:                                        l
                                                                                1
       Perform an engineering evaluation of the test results for CS pump
                                                                                '
 -
       2A-A and verify that test data is not indicative of possible pump
       failure,                                                                 j
 -     Discuss furth'st the need to scale control room indication using
       previous test risults.
  -
       Review the location of the Anubar Flow instruments and evaluate the
       possibility of any needed modifications.
  -
       Verify heat exchanger differential pressure ( D P '. during each
       Surveillance Instruction (51) or American Society for Mechanical
       Engineers (ASME) boiler Jnd pressure vessel code uction XI testing
       of the pump and determine an acceptable fouling fa: tor.
  Disposition of the four items is addressed below.                             ,
                                                                                l
  The pump test run, September 8,      1987, (2B-B) and September 11, 1987,
  (2A-A) indicates that the pumps are within manufacturer's specifications.
  The ultrasonic flow meter used during Surveillance Test Instruction
                                                                                l
                                                                                i
     ..-
 .
                                         21-
   (STI)-65 was approximately 1.9% low at the upper flow ranges used to
   determine flow characteristics.        This, in. conjunction with other data
   taken over a period of years would indicate that the 2A-A pump is still
   servicable.      The licensee's investigation of this matter appears to be
   adequate.                          -
   The need to scale control room indication was discussed with TVA and TVA
   may decide to mark flow indicators. However, there is no criteria to have              !
   a calibrated flow indication in control room. Only an indication of flow               ;
   is required.      The licensee's actions appear to be adequate.                      .l
                                                                                          l
   The location of anubar flow instruments and verification of heat exchanger             !
   differential pressure are long term issues which are not required to be                i
   completed prior to Unit 2 heatup or startup.         These long term commitment        {
                                                                                          '

,

   items will be addressed through review of the corporate commitment

i tracking system and will be followed with IFI 327, 328/87-76-04.

                                                                                          l
   The heatup requirements of this URI have been satisfied for Unit 2 heatup.
   This item is closed.
   (Closed) VIO 327/89-23-01, 328/84-24-01; Inadequate Corrective Action for

l Unconfirmed Piping Analysis Operational Modes Input . Data. This issue l involved a violation for inadequate licensee corrective actions for the l resolution of a Non Conformance Report. The licensee admitted the

   violation with clarification.         Prompt corrective action was taken to
   resolve the concerns expressed in NCR SQNCEB8205. However, the corrective              j
   action was not properly documented on the NCR, and the NCR had not been
   closed upon completion of the corrective action.           The licensee reviewed

l '

   the programmatic control over operational modes for SQN in May 1982. In
   addition, the adequacy of the SQN piping analysis was to be reviewed,                  1
   based on the Watts Bar Nuclear Plant (WBN) operational modes review.                   !
   These reviews were completed in February 1984, with no potential safety                i
    problems identified at SQN.       The licensee has signed all ENDES action            I
   complete on NCR CEB8205, R1, as of., December 26, 1984, and the Office of
    Engineering (OE) civil       discipline is tracking completion of the
    documentation of corrective action requirements via the Tracking and
    Reporting of Open Items (TROI) System. The licensee's actions appear to
    be adaquate.                                                                          l
                                                                                          i
   This item is closed.                                                                   i
    (Closed) VIO 86-68-02; Sample (17-1) Lack of Material Traceability
    Documentation for Diesel Generator Anchor Bolts. During the performance
    of a recent safety system outage modifications inspection (SSOMI) several
    anchor bolts were identified that did not have adequate material
    traceability to material specifications.          In response to this SSOMI
    violatio:, the licensee issued CAQR SQP870937 which required that samples
    of 28 of the 144 anchor bolts in question, be tested to determine their
    chemical and physical properties.          The results of these tests were
    evaluated and it was determined that the installed bolts are adequate to
    perform their intended function.        The inspector reviewed the above test

l

                                                 . .-        --      .
                                                                       .    --      . -
  . ..            _-        -        - -.                                   . .-             -   .       . -    - .
              .-
             r

'

              .
                      ,
                                                                     22
                     , results and evaiuation and determined that, as the reported chemical
       '                properties are comparable to those of the specified AISI 1141 material,
                        and the tensile strength is slightly greater than specified, the
         '~r
                        licensee's evaluation is appropriate and the installed anchor bolts are
                        acceptable.
                        This item is closed
                                                                                                                    I
                        (Closed) VIO 328/85-17-04; Failure to Follow Emergency Diesel Generator                     l
                        Surveillance Test Procedure. This violation is identical in technical
                        content and required corrective action to violation 327/85-17-05, which
                        was previously reviewed, determined to be acceptable, and closed in
                        inspection Report 327,328/87-17.
                        This item is closed.
                                                                                                                    l
                        (Closed) URI 327,328/87-23-01; Control of Safety Related Diesel Generator                   j
                        (DG) Spare Battery Components Beyond the Confines of a Designated                           I
                        Warehouse. Vital EDG battery cells were stored in the EDG building.                         I
                        Several of the cells could not be properly identified in the original
                        report. The loss of control of this material appors to be an isolated                       j
                        case stemming from the inability of power stores to maintain the batteries
                        in normal storage areas, and personnel error in that the transfer of the
                        material was not properly tracked.                The ~ inspector reviewed the storage      l
                        maintenance program for the spare bank of EDG batteries and finds that                      !
                        program to be adequate. Based on an adequate storage and maintenance
                        program, proper identification of the EDG spare batteries, and tagging of
                        8 batteries as defective to prevent use in safety related systems the
                        actions for this URI are adequate.
                        This item is closed.
'
                 4.     Operational Safety Verification (71707) Units 1 and 2
                        a.      Plant Tours
                                The inspector observed control room operations, reviewed applicable
                                documentation, conducted discussions with control room operators,
                                observed shif t turnovers, and confirmed operability of instrumenta-
                                tion.         Approximately twenty separate NRC tours were conducted of the
                                control room. Each tour consisted of- approximately two hours eacb.
                                In addition, approximately twenty shif t briefings and shif t turnovers
                                were audited. The inspector verified the operability of selected
                                emergency         systems,     and   verified    compliance with Technical
                                Specification (TS) Limiting Conditions for Operation (LCO).                  In
                                specific, TS 4.2 and 4.8 were reviewed in depth to ensure
                                operability.          The  inspector verified        that Maintenance Work
                                Request / Hold Orders had been submitted as required and that followup
                                activities and prioritization of work was accomplished by the
                                licensee. The following sources of information were reviewed to
                                ensure the appropriate documentation of plant conditions:
       . _ _                  _           . _ _ _            _     ,   __        _      _- .       _.,
 '
   .
                                   23
          . Shift Engineer Log, Assistant Shift Engineer Log, AI-6, rev. 13.
           Reactor Operators Log, Al-6, rev. 13
           Auxiliary Unit Operator Daily Shift Log, AI-6, rev. 13
           Temporary Alteration (TACF) Log, AI-9, rev. 25
           Hold Order-Log, AI-3, rev. 38
           Operator Aid Log, AI-6, rev. 13
           Configuration Control Log, AI-58, rev. 1
           PRO Log, AI-12, rev. 3
           S01-67.1, rev. 34, Essential Raw Cooling Water System
           S01-72.1 rev. 29, Containment Spray Systems
     Approximately 20 separate tours of TVA plant spaces were conducted.
     Tours were conducted in the diesel generator, auxiliary, control, and
     turbine buildings, and containment in order to observe plant
     equipment conditions (including potential fire hazards, fluid leaks,
     and excessive vibrations) and plant housekeeping / cleanliness condi-
     tions.    The inspectors walked down appropriate portions of the
     following safety-related systems on Unit 1 and Unit 2 to verify
     operability and proper valve alignment:
           RHR System

'

           Control Room Ventilation System
           Containment Hatch Covers
     The reason containment hatch covers were toured, was that on
     August 26, 1987, D.C. Cook (a sister plant to Sequoyah run by Indiana
     and Michigan Electric) determined that the reactor coolant pump hatch
     covers on Unit 2 could fail in the event of a loss of coolant
     accident. The hatch covers provide access from the upper containment
     to each of the reactor coolant pump areas in the lower containment,
     and serve as a divider barrier between the upper and lower
     containment in the ice condenser design.
     Indiana and Michigan Electric performed ultrasonic examination of the
     Unit 2 bolts holding the hatch covers in place. Their examinations
     determined that 25 of a total 74 bolts had been cut and welded (as
     opposed to 12-inch embedment in concrete) during the original
     installation.    The inspector discussed the issue with Sequoyah
     personnel and the licensee issued Nuclear Experience Review 870727 to
     investigate. The licensas visually inspected the bolting on Unit 2
     and UT inspected the bolting on Unit 1. No discrepancies were found.
     The inspector reviewed the documer.tation associated with these tests.
     Additionally, the inspector visually inspected approximately 25% of
     the bolting on Unit 2 hatch covers and found no descrepancies. This
     issue is closed.
     No violations or deviations were identified.
                                                                             ]

.

                                  24
 b. Safeguards Inspection
    The inspectors included a review of the licensee's physical security
    program. The performance of various shif ts of the security force was
    observed in the conduct of daily activities including protected and
    vital area access controls; searching of personnel and packages;
    badge issuance and retrieval; patrols and compensatory posts; and
    escorting of visitors. The inspectors also observed protected area
    lighting, as well as protected and vital area barrie* integrity.
    Additionally, The inspectors verified an interface between the
    security organization and operations or nisintenance; witnessed
    fi rearms training and qualification; responded to bomb threats,
    fires,    etc.;   interviewed individuals with security concerns;
    participated in offsite support agencies visit to facility; inspected
    security during octages; reviewed licensee Security Event Reports;
    witnessed spent fuel shipment; visited central or secondary alarm
    station; witnessed power supply test; verified protection of
    Safeguards Information;      verified onsite/offsite communication
    capabilities; and witnessed Corporate annual audit of site security
    program.
    Security Incident PRO-1-87-438, was reviewed and its contents were
    discussed with NRC Region II Security Specialists.
    No violations or deviations were identified.
 c. Radiation Protection
    The licensee's Health Physics (HP) and Radiological Protection
    Programs were observed. Included in this observation were radiation
    protection controls, use of protective clothing, and proper use of
    radiation protection instrumentation.         The   inspector verified
     implementation of radiation protection control.         Specific work
    activities were monitored to ensure the activities were being
    conducted in accordance with applicable RWPs.         Selected radiation
    protection     instruments were verified operable and calibration
     frequencies were reviewed.    The following occurrences were reviewed
    by the inspectors:
    (1) On December 9,1987, the licensee informed the resident staff
          that there was possible Co-60 contamination in the west septic
           tank of the plant sewage treatment system. This sewage treat-
          ment system is not designed to process radioactive waste and is
          not physically connected to any plant operating system.         In
          September the licensee had discovered trace amounts of I-131 in
           this tank and had traced its origin back to an employee who had
           received an I-131 medical injection.     The Sequoyah units have
          been in mode 5 for over 2 years and, therefore, because of the
           short halflife of I-131, plant systems do not presently contain
          detectable levels of I-131.
   __    . _ _ _ _         _                 .  .          _
      =
                   .
                                                        25
                               Following the detection of I-131, the licensee began sampling
                               selected tanks on a routine basis. In late November, plant
                               chemistry personnel detected indications of approximately 1 x
                               10-7 p Curies /cc Co-60 in the west septic tank.       Additional
                               sampling indicated a maximum concentration of about 1 x 10-6
                               y Curies /cc Co-60.
                               On December 8,     1987, per sewage plant operations procedure,
                               sewage plant personnel pumped a partial load of sewage from the
                               equalization tank into a contractor's truck and shipped it
                               offsite.    This equalization tank is the collection tank for the
                               sewage prior to sending it to either the east or west septic
                               tank. Shortly after the shipment left the site, plant chemistry
                               personnel postulated that the shipment may contain Co-60, based    ;
                               on Co-60 indications in the west septic tank. A sample was
                               taken from the equalization tank and Co-60 was indicated.      The
                               licensee immediately took the same sample to a separate
                               licensee-owned offsite counting laboratory.      No indication of
                               Co-60 was detected in the same sample at the offsite counting
                               laboratory. On December 10, 1987, the licensee detected Co-60
                               in higher concentrations on a laboratory count blotter used to
                               transport samples within the onsite laboratory.
                               Additional samples were taken and no Co-60 was detected in the
                               equalization tank or either septic tank. The licensee is
                               reviewing their laboratory counting technique and the sewage
                               disposal program. This event will be reviewed by an NRC Region
                               II specialists.
                          (2) On December 12, 1987, while reviewing the RWP for_ entry into the
                               Unit 2 upper containment, the inspector observed several workers
                               frisking af ter exiting from the annulus.      One worker, while
                               frisking, accidentally dropped the pancake probe to the floor.
                               He retrieved the probe and continued frisking without further
                               checking to ensure the equipment was operating. Investigation
                               by the inspector revealed the frisker to be damaged and not

, operating. The inspector pointed out the damaged frisker to the i

                               HP technician who immediately removed the frisker from service.

'

                                                                                                  '
                               The technician stated that frisking when exiting from the
                               annulus was not absolutely required and no further followup        i
                               action was initiated by the licensee.       The inspector had no
                               further questions.
        5.           Engineered Safety Features Walkdown (71710)
                     The operability and proper lineup of plant system , is addressed in special
                     NRC team Inspection Reports 327,328/87-66 and 88-06.
                                                                                                  l
                                                                                                  !
 -                                .-      ._                  . - _ _ - .  -
                                                                                -.      .  .
 ,_ .          -       . - . - -         .            .
                                                                                           i
      0
           .                                                                               :
                                                                                           I
                                                  26                                       l

,

        6.   Monthly Surveillance Observations (61726)
             The inspector observed / reviewed the below listed TS required surveillance
             testing, special tests and postmaintenance/ modification tests.          The
             inspector verified that testing was performed in accordance with adequate
             procedures; that test instrumentation was calibrated; that LCOs were met;
             that test results met acceptance criteria requirements and were reviewed
             by personnel other than the individual directing the test; that
             deficiencies were identified, as appropriate, and that any deficiencies
             identified during the testing were properly reviewed and resolved by
             management personnel; and that system restoration was adequate. For
             completed tests, the inspector verified that testing frequencies were met
             and tests were performed by qualified individuals.
                   SI-1, Surveillance Program; The inspector noted no deficiencies with
                   the portions observed.
                   SI-40, Centrifugal Charging Pump; The inspector noted no deficiencies
                   with the portions observed.
                   51-265.0, Hydrostatic Testing; The inspector reviewed the completed
                   Hydrostatic test package associated with WRs B240532, B240533, and
                   B251598, which replaced three sections of ERCW piping that had been
                   removed because of MIC-induced leakage.     No problems were noted.
                   SI-691, Spent Fuel Pit Pumps; The inspector noted no deficiencies
                   with the portions of the test that were observed.
                   SI 153.4, Revision 2, Test Requirements for the Electric Hydrogen
                   Recombiner System, Unit 2; The purpose of this SI is to verify
                   operability of the Unit 2 Hydrogen Recombiners. This SI is performed
                   every 18 months and consists of a visual inspection, electrical
                   checks and operation of the recombiners. The inspector at:ompanied
                   the maintenance personnel during portions of the 28-B recombiner
                   attachment of this SI.       The prerequisites require that SI-153.1,
                   Periodic Calibration of Hydrogen Recombiner System Instrumentation,
                   be completed; SI-151, Six Month Test Requirement on Electric Hydrogen
                   Recombiner System, be performed just prior to this SI; and hold
                   orders obtained prior to performing visual and resistance to ground
                   checks. The hold order was properly placed and the Assistant Shift
                   Engineer (ASE) signed for the completion of SI-151.        However, no
                   verfication signature for completion of SI-153.1, as detailed in the
                   prerequisites, is required in the procedure and there is no clear
                   understanding of what "just prior" means for SI-151.        These are
                   typical SI administrative deficiencies which are to be remedied in
                   the second phase of the licensee's SI review program.                   l
                   The Maintenance electricians (ME) verified the hold order tags in
                    place and checked the load side of the power supply de-energized.
                   The ME then performed the electrical resistance to ground checks.
                   Al thot.g h the readings obtained met the acceptance criteria the
                   behavior of the test instrument was suspect.      The reported behavior
                   was not similar to that observed on the 2A-A recombiner. The test
                                 . _ _ .      -   -     .          _
                                                                      .   -_
       _. - -                   -        -       -       -         .                          .  -
              *          .
                                                                27
                                                                                                                  '
                                instrument was in calibration, however, it was a different instrument
                                than the one used for the 2A-A checks. This situation was resolved
                                by selecting a better suited instrument from those specified in
                                Instrument Change Form (ICF) 88-093.
                                A loose bolt or support rod was identified .inside. the recombiner
                                ho; sing. The function of this item was unclear after reviewing the
                                vendor manual. A work request was written by the ME. Two' procedural
                                discrepancies were identified.               The first involved verifying the
                                orifice at the bottom of the housing clear of obstruction per step
                                5.3.4 of SI-153.4. The ME did not understand what was required for
                                the inspection of the orifice. Prior to conducting the 2B-B portion
                                of the SI the ME had requested clarification of the step from the
                                cognizant engineer and it was determined by the ME that the orifice
                                was an exterior louver. However, subsequent review of the vendor
                                manual      by the NRC inspector, revealed an orifice plate, at~the
                                bottom of the heater banks.          As a result of the NRC inspector's
                                 finding, the ME returned to the 28-B recombiner to inspect the
                                orifice plate clear of obstruction.               The inspector did not observe
                                 this re-inspection.

, The second discrepancy involved a visual inspection of the wiring

                                  from the ring terminal in the main junction box to each heater bank.
                                The ring terminals in the main junction box are covered with Ray chem
                                 heat shrink and cannot be inspected without removal of the heat
                                  shrink. Removal of the Ray chem heat shrink was not performed during
                                 this SI. The inspection of the wiring to each heater bank is unclear
                                 as it would require disconnection of wires and removal of an addi-
                                  tional panel for access.       The procedure does not provide for
                                 disconnecting terminals and the actual connection to each heater bank             ,
                                 was not inspected. The ME, have asked for a clarification.                        l
                                  Previously, on December 14, 1987, the ME had ' inspected the 2A-A
                                  recombiner orifice plate; a loose bolt, similar to the one in 2B-B,
                                 was found. A work request was written to resolve the loose bolt in
                                  recombiner 2A-A. The inspector reviewed Westinghouse Technical
                                  Bulletin (TB) NISD-TB-85-08, EHR Cable Inspection, provided by the
                                  licensee on December 14, 1987. The TB detailed the inspection
                                  recommendations of the vendor for the main power cable visual checks.
                                  The inspector believes visual inspection as specified in SI-153.1 and
                                  as observed during the conduct of this SI is sufficient to comply
                                 with the recommendations of the TB even though the visual inspection
                                  as outlined in the SI was not adequately implemented.
                                  The licensee failed to adequately implement SI-153.4 in that the
                                  requirement of step 5.3.4 to visually verify the hydrogen recombiner
                                  orifice clear of obstructions was not properly conducted prior to                !
                                   signing the step as completed due to inadequate management
                                  supervision provided to the personnel performing the SI.                This is
                                   identified as second example of VIO 327/328/87-76-02.                A second
i
                                  example of this violation is located in paragraph 9 b of this report.
                                                                                                                    l
                                                                                                                    l
  .- .
                _ _ . _ . - ..-               ..     .     . __
                                                                     . .- ._
 . ,
                                     28

'

     STI-68, Refueling Water Storage Tank Heater Control Logis Cunctional
     Test; The inspector reviewed STI- 68, Unit 2, Revision 0.      'he scope
     of STI-68 was to verify the control logic of the Unit 2 Refueling
     Water Storage Tank (RWST) immersion heaters C and D, verify operation
     of the cold leg accumulator nitrogen header vent valve from the
     Auxiliary Control Room, and verify proper operation of the cold leg
     accumulator nitrogen header pressure control valve 2-PCV-63-58. The
     test procedural steps were clear and understandable.        Acceptance
     criteria were stated for attributes to be tested.          Inspectors
     concluded the test was adequate for performance as written.          The
     following observations were discussed with the TVA staff:
     -
           Section 6.5 of the test relating to the nitrogen header vent
           valve and nitrogen accumulator header pressure control valve is
           not related to sections 6.1 through 6.4 of the the test. TVA
           staff indicated that section 6.5 was added for ease of review
           and approval.
     -
           In test section 3.5, the absence of a red indicator light is
           used as indication that RWST heaters are not energized. As the
           purpose of this special test is to verify proper heater logic, a
           more positive indication that heaters are not energized should
           be used. NRC inspectors inspected several panels in the plant
           including the Chemical and Volume Control System 480 volt boards
           and found the following red indicator lights had missing bulbs:
                 480 Volt CVCS Control Board A
                       Breaker 2D - RWST Immersion Heater A, Unit 1
                       Breaker 3C - Caustic Batching Tank Mixer
                       Breaker 2B - Evap Cond Drain Pump A
                 480 Volt Aux Building Common MCC A
                       Breaker 2D - Transformer A Exhaust Fan
                       Breaker 2E - Transformer Exhaust Fan
                       Breaker 50 - Pri Cig Wtr Loop Pmp B
                 480 Volt Aux Vent Board 2Al-A
                       Breaker 7A - 480 Bd Rm 2A Pzr Fan 2Al-A (bulb was out
                       of socket loose in indicator).
            Inspectors gave the list of indicators with missing bulbs to the
           Shift Supervisor for correction.
      -
           Drawing 47W830-6, Mechanical Flow Diagram Waste Disposal System,
           Revision 8, contains an error in zone A-1.       The continuation
           drawing for the high pressure nitrogen header that is referenced
            is in error. This was turned over to the test coordinator for
            transfer to drawing control . A drawing discrepancy form had
 ,
                                29
        been submitted to drawing control previously by TVA personnel.
        The drawing error did not affect the outcome or adequacy of the
         STI and was not safety significant.
   SI-15, Emergency Core Cooling System Loop 4 RCS Isolation; This
   surveillance tested RHR Isolation valve operation - and interlocks
   associated with RCS pressure on Loop 4. Test personnel conducted a
   walkdown prior to the test and found errors in switch numbering.
   This was corrected with an instruction change form prior to the test.
   No deficiencies were noted.
   SI-97.2, Calibration of Auxiliary Feed-Water Flow Rate for Remote
   Shutdnwn and Accident Monitoring; No deficiencies were noted during
   the performance of this surveillance.
   S1-144.2, Control Room Emergency Ventilation Test; The inspector
   reviewed the SI and observed portions of the performance of SI-144.2
   on December 18, 1987, on the A train of the control room ventilation
   system.    This test is performed at an 18 month interval and is
   intended to verify that the control room emergency ventilation system
   maintains the control room at a positive pressure of 1/8 inch of
   water gauge relative to the outside atmosphere at a cleanup flow rate
   of 4000 + 10% cfm. Additionally, the SI is intended to verify that
   on a high radiation signal from the air intake stream, the system
   automatically diverts its inlet flow through the HEPA filters and
   charcoal absorber banks. The inspector reviewed ICF # 87-2386 and
   the~ associated USQD for SI-144.2. This change allowed performance of
   the test without smoke testing doors C53 and C60 until replaced under
   ECN L6860 as implemented by Work Plans 12602 and 12604. A new
   temporary boundary has been established in the Unit 2 stairwell to
   the control room which temporarily relocated the control room
   pressure boundary.
   The inspector observed the initiation of the train A control room
    isolation at the control room ventilation radiation monitor,
   RM-90-125, in the mechanical equipment room.           The indicated
   differential pressure shown on the temporarily installed inclined
   manometer had stabilized at about .21 inches of water within 30
    seconds of the initiation signal. However it was discovered during
   the test that the Unit 2 control room stairway door, C-25, was
   breached affecting results.     With the door closed a less positive
   pressure resulted and the system failed to provide the required 1/8
    inch of water positive pressure. The licensee is continuing with the
    performance of Special Test Instruction (S11) - 83, Rev. O, Control
   Building Emergency Pressurization which consists of a ventilation
    flow balancing involving obtaining data which would allow
   determination of flow path and alignment changes necessary to resolve
    control room inleakage/ pressurization problems. Additionally the
    licensee is investigating'different corrective action plans.
       .
                                            30
                                                                                     1
         *
             STI-83, Rev. O, Control Building Emergency Pressure Ventilation Test;
             The inspector reviewed the incomplete package for STI-83. This
             ongoing test consists of a ventilation system flow balancing-
             operation and obtaining data which would allow determination of' flow
             path and alignment necessary to resolve inleakage and pressurization
  ,
             problems identified in CAQR SQP871226 Rev. 1. The licensee is            ,
5
             planning on continuing with this test until the system will support      !
             successful completion of SI-144.2, Control Room Emergency Ventilation
             Test.
    7.   Monthly Maintenance Observations (62703)                                     '
                                                                                      '
         a.  Station maintenance activities of safety-related systems and compo-
             nents were observed / reviewed to ascertain that they were conducted in
             accordance with approved procedures, regulatory guides, industry
             codes and standards, and in conformance with TS.        In addition an
              individual review was conducted of each restart WR existing on the
              licensee's daily work list on a weekly basis. The total outstanding
              restart WR number was approximately three hundred on January 18,       ;
              1988.   The licensee's maintenance planning activities were also        !
              observed on a daily basis,
         b.  Attributes considered during a review of work requests (WRs)/ work
              plans (WPs) were that: LCOs were met while components or systems        i
             were removed from service; redundant components were operable;
              ar,     is were obtained prior to initiating the work; activities were '
                  *
              i         shed using approved procedures and were inspected as
                r    ;sle; procedures used were adequate to control the activity;    l
              trouoleshooting activities were controlled and the repair record       -
              accurately reflected what actually took place; functional testing
              and/or calibrations were performed prior to returning components or
               systems to service; quality control records were maintained;          t
              activities were accomplished by qualified personnel; parts and          r
              materials used were properly certified; radiological controls were     '
               implemented; QC hold points were established where required and were   ,
              observed;    fire prevention controls were implemented; outside         '
              contractor force activities were controlled in accordance with the
              approved Quality Assurance (QA) program; and housekeeping was
              actively pursued.    The following WRs were reviewed:
                    WR B-242678
                                                                                       l
                    WR B-231942                                                        l
                    WR B-232394; The inspector observed portions of the removal of
                    the A refueling water purification pump foundation and instal-
                    lation of new foundation. The old foundation was removed and
                    repositioned to a lower location to allow alignment of a new
                    pump / motor. The foundation grout was replaced per M&AI-17.
                                                                                       l
                                                                                     ;
                 ..    .       -.- - - .              -           - - - _                                     .-        -                                -
              =
                       .
                                                                                31
WR B-208086; The inspector followed the progress of the work-
                                           associated with . repairing the valve cover gasket leak on the
                                           Unit 2 RHR suction check' valve, 2-63-502. The gasket leak had
                                           resulted -in a buildup of boron precipitate around the cover
                                           bolting and the exterior surface of the valve body which could
                                           result in deterioration of the valve cover bolting.                                                           The work
                                           request had originally been planned to disassemble the 12-inch
                                           check valve, replace gasket, clean and inspect for any defective                                                                                 ,
                                           components and reassemble the check valve. This work as planned
                                           would require taking both trains of RHR out of service and was
                                           to be performed as part of a scheduled RHR outage. However, the
                                           WR was replanned to allow the cover bolting to be retorqued per
                                           MI-6.15, Rev.14, General Procedure Tightening Bolted Joints.
                                           The check valve surfaces were cleaned and the valve cover was
                                           checked for further leakage at different RCS pressures up to and
                                           including 350 psig. No leakage was noted and the WR was placed
                                           on a planning hold pending final evaluation by the licensee,
                           c.        The licensee has had control difficulties with clearance orders in
                                     the recent past. As a result, the licensee has recently implemented
                                     a clearance /ta;3ing group to relieve the administrative burden on the
                                     ASE associated with these activities. The purpose of this group is
                                     to review work requests for adequacy and tagging requirements. The

'

                                     group is also responsible for hanging / clearing tags.                                                          The group
                                     appears to be a positive step. However, it is newly implemented and
                                     its effectiveness is yet to be determined. The group is presently
                                     active only on the day shift.                                                                                                                          ,
                           No violations or deviations were identified.
                    8.      Licensee Event Report (LER) Followup (92700)
                            The following LERs were reviewed. The inspector verified that: reporting                                                                                         i
                            requirements had been met; causes had been identified; corrective actions
                            appeared appropriate; generic applicability had been considered; the LER
                            forms were complete; the licensee had reviewed the event; no unreviewed

i safety questions were involved; and no violations of regulations or

                            Technical Specification conditions had been identified.
                            (Closed) LER 327/87-057;                      Control                 Room Isolation Initiated During
                            Performance of a Special Test Instruction.                                           During the performance of
                            STI-30, DC High Voltage Test for Selected 1E Cable With Potential For
                            Cable Pullby Damage For Conduit MC 1607A, the door to local junction box
                            0-L-450 was opened and a control room isolation was initiated.                                                                     The
                            junction box is the control room chlorine detector panel. The inspector
                            reviewed the LER and the associated PRO (PRO 1-87-305). The licensee
                            attempted to reproduce the event by opening the junction box. However, a
                            recurrence of the event could not be initiated.                                                 The licensee also
                            inspected the junction box for loose or damaged connections.                                                                                                     l

.

                            This LER is closed.
                                                                                                                                                                                             I
 , - - - , , - -        , ,       -.     -
                                                  n     .---....m             , , - - . . , , - - . , - . _ _          . - - . _ - . - - . ..-.,.~._,.my   ,m. . , , . , - , - . . . -- .n,
                    _.      _   _        ._ _          .__ ~        . _.             _                .      . ..
         -
             .
                                                          32
               (Closed) LER 327/87-064: Improper Fit of Emergency Raw Cooling Water Flood
               Mode Spool Pieces Due to Minor Piping Orientation Changes. This involved                           ,
               an issue identified in the NRC Integrated Design Inspection (IDI) for the                          '
               Emergency Raw Cooling Water (ERCW) system that found that flood mode spool
               pieces did not properly line up.                The root cause appears to be a
               combination of system modifications and pipe stresses over the cperating
               years.     The licensee committed to performing a piping analylis by
               December 2,1987, and to have the spool pieces codified to ensure proper
               fit by January 1,1988. The licensee has reviewed all spool pieces and
               identified thirteen spool pieces for Units 2 and 3 spool pieces for Unit 1
               that require modification. These have been modified per work procedure
               (WP) numbers 12735 (Unit 2) and 0082-01 (Unit 1). The piping analysis has
               been completed per calculation package N2-IDI-SP00L-MISC.               The long term
               corrective action to prevent future misalignment is being tracked by
               corporate con'mitment tracking system (CCTS) items NCO 870350 003 and NC0
               87 0350 004, The licensees actions appear to be adequate.
               This LER is closed.
               (Closed) LER 327/87-069; Failure to Satisfy A Containment Spray Pump
               Surveillance Requirement.           This issue involves SI-247.900, Engineered
               Safety Feature Response Time Verification, which did not require the
               complete containment spray pump control circuitry               (i.e., pump start
               contact) to be included in the response time testing.              Furthermore, the
               valve start time was not included in the overall calculation.                   The
               Licensee has committed to revising SI-247.900 by completing tests using
                instrument maintenance instruction IMI-99 response test RT-643 A and B,
               "Response Time Testing, Engineered Safety Features, Slave Relay K 643",
               prior to Mode 4 operation of Unit 2.                 The inspector verified that
               SI-247.900 had been revised. This was accomplished by instruction change
                form (ICF) 82-2140. IMI-99 and RT643B have been completed through the
               November' 18, 1987 performance of SI-247.100B (Train B, Unit 2) and the
               Novmeber 12, 1987 performance of SI-247.100A, (Train A, Unit 1). A
               preliminary review of the test results indicate that the response time
               will meet TS.      The Licensee's actions appear to be adequate.
               This LER is closed.
                (Closed) LER 327/87-066; Potential loss of Component Cooling Water

, Inventory Due to Non safety Related Design of the Pump Seal Leakage Return

                System.    This issue involved a determination by the licensee that the
                component cooling water system (CCS) pump seal leakage could deplete the
                CCS water inventory in approximately 52 hours following a loss of coolant
                accident (LOCA), assuming two CCS pumps running in the same train and a
                loss of of f-site power. A review of the appropriate abnormal operating-
                instructions (AOI) indicated that the problem had not been addressed and                           i
                procedures were not in place to mitigate the condition. The licensee has
                revised the system operating instructions (S0I)-55-0M278-XA-55-27B-C
                (approved     January 17, 1988), (501)-55-0M27B-XA-55-27B-0 (approved
               January 17,1988) and A0I-15 (approved January 18,1988) and has committed                            j
                to update the Final Safety Analysis Report (FSAR) to allow entry into the                          j
                                                                                                                   l
                                                                                                                   l
 - . - -   -
                  - . - -            .        ,- .           ,   --       _.               -         - - - -
 . _ _ _ _ _ _ _ . _ _ _. . -                        . . .
                          *   ,
                                                                       33
                                auxiiiary bdiding to install the cross-over spool piece to connect the
                                emergency raw coJ)ing water (ERCW) to the CCS. This is being tracked by
                                corporate cemmitment tracking system (CCTS) item NCO 87 0351001. The
                                 licensee's ccticas appear to be adequate.
                                This LER is closed.

l

                                 (Closed) LER 327/87-048; Failure' of Silicone Rubber Insulated Cables
                                 During High Voltage Testing. This issue involved testing of worst-case
                                 low voltage vertical drop cables subjected to a high potential test of
                                 10,800 volts. 3 out of 16 conductors had inadequate dielectric strength
                                 to withstand that voltage level." A review of the licensee's corporate
                                 commitment tracking system (CCTS) indicates the following:
                                 (1)    Failed silicone rubber cables have been replaced CCTS no. NC0 87 0322
                                        001 (closed).
                                 (2)    Requirement to perform . additional test and analysis has been
                                        committed to CCTS, no. NCO 87 0322 002.
                                 In a telephone conversation with OSP Management January 19, 1988, it was
                                 stated that the NRC would accept the testing to date, for restart and
                                 operation, until the next refueling outage; at which time they would ask
                                 for sample cables to be pulled and verification tests implemented on the
                                 samples. The licensee has ccmleted item 1 and is tracking item 2. The
                                 licensee's actions appear to bs adequate.
                                 This LER is closed.
                                 (Closed) LER 327/87-010; Numerous Relays, Level Switches, Cycle Timers,
                                 Load Controllers, and Meters Have Not Been Calibrated Because They Were
                                 Not Identified in Procedures. This issue involved a lack of clearly
                                 defined departmental responsibilities that allowed components, requiring
                                 calibration on a routine basis, to be lef t out of the calibration cycle
                                 when department prepared calibration procedures are within their
                                 jurisdiction.       The licensee has developed a series (13.1 and 13.2) of
                                 maintenance instructions (mis) to cover all the components identified as a
                                  result of a Division of Nuclear Quality Assurance audit. The mis and
                                 Preventive Maintenance (PM) procedures have been approved and are issued.
                                 The components required to be calibrated prior to restart have had issued
                                 and completed. The licensee's actions appear to be adequate.
                                                                                                                       !
                                 This LER is closed.
                                  (Closed) LER 327/87-045; An Inadequate Design Control Process Resulted in
                                  the lack of Fuse Coordination Potentially Rendering the ERCW System
                                  Inoperable. This issue involves engineering change notice (ECN) L5637,
                                 dated February 17, 1983. This ECN added a fuse to each of the four                    l
                                  essential raw cooling water system (ERCW) traveling screen speed switches
                                  to isolate the non-class 1-E speed switches from the class 1-E control
                                  circuit.    An     inadequate design control    process did not require
                                                                                                                       i
          ,                -.  .                   -        -    -.-                      _   _ - . _ .     . _ . _ _,
 ._      . _              _ -          _.   _                                        _                              _
      -
              .
                                                      34
                calculations to be made to determine the type of fuses required to protect
                 the class 1-E control system. The licensee has issued design change
                 notice (DCN) 00078c, dated October 24, 1987, to document the fuse
                 requirements necessary to ensure proper coordination between the class 1E
                 and non-class IE portions of the ERCW traveling screen electrical circuits
                 and to install the proper fuses prior to mode 4 operation.
                 The inspector has reviewed DCN 00078c.        The fuses in question have been
                 evaluated by the licensee and replacement fuses have been installed per
                work package (WP).12725. DCN 00078c will not be closed until the config-
                 uration control drawings (CCDs) have been issued; tentative issue date
                January 8, 1988. This DCN is in the process of being revised to allow
                   substitution of fuses and to clarify issuance of CCDs.       Sequoyah engi-
                  neering project (SQEP)- 09, Change Review Checklist for Electrical
                 Calculations, has been revised (approval date May 2, 1987) to require                                i
                  evaluation of each design change with electrical involvement. The
                 modification group has completed the modifications to the equipment
                   referenced in drawings 35W736-1, 35W736-3, 35W736-5, 35W736-7, 35W746-1,
                   35W746-2, 35W746-3, and 35W746-4.     The DCN has been delivered to the DNE
                  drawing unit (DDU) which has six months in which to update the drawings
                   per Administrative Instruction (AI)-19, revision 25, paragraph 4.5.2.        The
                   licensee's actions appear to be adequate.
                   This LER is closed.
                   (Closed) LER 327/84-59; Failure To Comply With Appendix R of 10 CFR 50.                             ,
                   This LER report was the result of inspections of various safety-related                             j
                   systems and details specifics of installations not .in compliance with 10
                   CFR 50, Appendix R. The issues involved inadequate lighting for safe
                   shutdown with the control roem inaccessible, overflow of the Reactor
                   Coolant Pump "pocket sump" upon a failure of an oil pump, and numerous
                   instances of inadequate interaction separation between opposite train
                   components.    NRC inspection report 327,328/87-41 reported that the
                   licensee, had in Enclosure 5 to their December 21, 1984, submittal,
                   analyzed the Appendix R discrepancies identified in the subject LER and
                   identified the appropriate corrective actions to resolve the discrepancies
                   in Interaction Studies 22 through 27, 30, and 34. The licensee also                                 i
                   requested and was granted a deviation to Appendix R, Section III.G which                            !
                   was necessary as a result of corrective actions. The NRC issued an SER                              I
                   granting the request on May 29, 1986. NRC inspection report 327,328/87-41
                   reported this LER open pending completion of 182-B and 2A2-A 480V shutdown
                   board room cable tray water spray system installations.         NRC inspectors
                   reviewed this LER, NRC inspection report 327,328/87-41 and Work Plan
                   12285. Work Plan 12285 completed modifications to the fire protection
                   system for 182-B and 2A2-A 480v shutdown board rooms.
                   This LER is closed.
                   (Closed) LER 327/86-039; Surveillance Requirements not Performed Because
                   of Inadequate Procedures. This LER 7 ported that procedures were not

, adequate to test all interlock functions of the reactor trip system

    .  .     - - -      _     -      _                            . - _ _  __   ._ _           .    _ _ _ _ _ _ ~ _
 ~. . . _ - . -        _     - _.                 .      . ._       -    -            -.         .
             -
                .                                                                                  i
                                                         35
                                                                                                   :
                  interlocks,       reactor trip, P-4 permissive (Technical Specification
                  4.3.1.1.2,      table 3.3-1, 22G) or to test the ice condenser inlet door
                  position at the local panel during the functional test (Technical
                  Specification 4.6.5.3.1). NRC Inspection Report 327, 328/87-65 closed the
                  ice condenser inlet door portion of the LER and reported that a draft TS
                  interpretation had been written to define the boundary of the ~ total
                  interlock function.         The function in question testing of the main
                  feedwater valve closure on low reactor coolant system average temperature
                 with reactor trip) was being tested by procedure, but not by surveillance
                  instruction.         The draft Technical Specification interpretation, log
                  No. 94, Revision 1 was approved by plant management and issued on

, November 12, 1987. The inspector reviewed the interpretation and

                  concluded that action on this portion of the LER is adequate.
                  This LER is closed.
                  (Closed) LER 327/87-054; Technical Specification Required Action not Taken
                  with Both Control Room Isolation Radiation Monitors Inoperable Due to

,

                  Required Testing and a Design Deficiency. Control room radiation monitor
                  RM-90-126 was taken out of service to perform SI-83, Channel Calibration
                  for the Radiation Monitoring System. The monitor was taken out of service
                  on August 10, 1987. The surveillance requirement was due on August 12,
                  1987. This date included the allowable extension for an 18 month surveil-
                  lance. Radiation monitor RM-90-125 was also inoperable at that time due to
                  high voltage special testing that was being conducted. With both trains
                  inoperable, TS Limiting Condition for Operation (LCO) 3.3.3.1, action b,
                  requires initiating and maintaining control room emergency ventilation in
                  the recirculation mode of operation within one hour.         This could not be

j done as both trains of the control room emergency ventilation were "

                   inoperable pending resolution of a design deficiency previously reported
                  by LER 327/87-039.          The inspector reviewed the LER and supporting        ,
                  documentation and interviewed TVA instrument maintenance and plant
                                                                                                   '
                  operating review staff (PORS) personnel to evaluate root cause and
                  corrective action.        The surveillance package for RM-90-126 was issued in
                  March 1987, six months in advance of the surveillance due date.            An
                  extensive SI adequacy review during the same time period determined that
                  SI-83, Channel Calibration for Radiation Monitoring System, required             .
                   revision prior to performance of the surveillance.        The SI was reissued   ,
                  and the actual surveillance commenced on July 23, 1987, and was completed        '
                  on August 10, 1987, two days prior to the overdue date. Licensee action
                  appeared adequate.
                  This LER is closed,
                                                                                                   t
                   (Closed) LER 327/87-039, Control Room Emergency Ventilation System Single
                   Failure Criteria Violated Due To A Design Error Which Could Result In
                   Exceeding Allowable Dose To Operators. During performance of SI-144.2,          ,
                   Contrni Room Emergency Ventilation Test, the licensee identified a
                   potential for a single failure of the main control room normal
                   pressurization system to allow entry of unfiltered air into the control
                   room during control room emergency ventilation after a control room
                                                                                                   :
                                                                                                   I
                                     -
                                                                                                   i

.

                                     36
 isolation.     The discovery resulted in both trains of control room
 emergency ventilation being declared inoperable and entry into the
 associated TS action statement to suspend actions that would result in
 positive reactivity addition to the core. The LER reported that the root
 cause of this deficiency was under investigation along with corrective
 action and that a supplemental report would be submitted by December 4,
 1987.    Revision 1 to LER 87-039 was submitted on November 25, 1987, and
 revised the date to read "A supplement to this report will be submitted
 within 30 days following Unit 2 restart."        The revised LER did not
 address system operability and planned action to restore the system to an
 operable status prior to Unit 2 restart.
 The inspector reviewed the original LER, Revision 1 to the LER, all CAQRs,
 PR0s, the Technical Specifications, and the FSAR.          The inspector
 interviewed the TVA staff regarding present status of the Control Room
 Emergency Ventilation system, root cause determination, planned temporary
 corrective action prior to Unit 2 restart and permanent corrective action.
 The licensee's staff reported that the system was still inoperable.
 Corrective action had been taken to correct the single failure criteria
 problem reported in the LER 87-039, revision 0.     However, the system had
 failed the surveillance (SI-144.2) due to an inability to meet minimum
 pressurization requirements.      Attempts were in progress to improve
 weatherstripping and investigate ductwork improvements and then to retest
 the system in accordance with the surveillance instruction. Parallel
 action was in progress to pursue a change to the TS and FSAR based on a
 re-analysis uf the dose to control room operators with an increased          .
 pressurization flow of outside air. This was being pursued in the event      l
 that improvements to the system did not result in an operable system.        1
 Plant Operating Review Staff indicated that a second revision to LER
 87-039 was being prepared to report correction of the single failure         l
 criteria problem and corrective action planned to allow Unit 2 restart.
 The inspector discussed LER detail and content with licensing and PORS
  staff as the original LER reported the system inoperable and the revised    i
  LER reported that the root cause and corrective action would not be
  reported until 30 days after Unit 2 restart. Inspectors discussed the
  potential for needing prior NRC approval if changes were made which would
  affect the system design bases, assumptions, or analysis as detailed in
  the FSAR.    This would be particularly true if pressurization was to be     I
  increased by increasing the introduction of outside air. The resolution      l
  of Control Room Emergency Ventilation system issues is discussed in
  paragraph 15 of this report.
  This LER is closed.
  (Closed) LER 327/87-003; Potential For Loss Of Containment Air Return Fan
  Due To A Design And Construction Deficiency. This report describes the
  possible failure of air return fans installed between upper and lower
  containment areas due to containment spray water draining into the fan
  intake opening following a design basis accident. This condition resulted
  from an inadequate design of curbing and the failure to install / reinstall
  curbing on the operating deck. An additional problem was identified in
 - - -.. ..              _.    . .-                       .       ..          . -           - .

, '

            .
              ,
                                                    37
                that the containment air return fans would remove entrained water from the.
                containment atmosphere and divert it outside the crane wall, thus lowering
                the reactor sump water level and potentially affecting suction head
                requirements of residual heat removal and containment spray pumps.
                Additional notification of these conditions and the licensee's evaluations
                and corrective actions were provided to the NRC by a letter dated July 8,
                1987.    Corrective . actions included installation of curbing on the
                operating floor and in accumulator rooms 3 and 4, installing drain lines
                from accumulator rooms 3 and 4 to the inside of the- crane wall, revision
                of the containment spray system design criteria and the FSAR, and revision
                of SI - 19 to provide for inspection of the removable curbing on the
                operating floor prior to entry into Mode 4.
                The inspector reviewed the licensee's corrective actions to date and
                considers that the actions taken are adequate to support Unit 2 startup.
                The physical modifications have been completed on Unit 2 and SI-19 has
                been revised. Written commitments for design criteria and FSAR changes
                have been issued and have been verified to be present in the licensee's
                CCTS.
                This LER is closed.
                (Closed) LER 327/87-006; Operation of All Equipment Affected By Manual
                Safety Injection Test Was Not Verified Because Of Deficient Procedures.
                The licensee's review of sis identified numerous equipment functions that
                were not being verified as required during tests involving manually
                 initiated safety injection signals. The inspector reviewed revised
                 SI-26.1A and SI-26.2A, Loss of Offsite Power With Safety
                 Injection-Containment Isolation Test, and determined that the previously
                 omitted verifications were now included. These function verifications
                 have been satisfactorily completed in accordance with the revised sis in
                June and October 1987. The licensee's extensive program to review all sis
                 and improve procedure preparation controls should prevent recurrence of
                 this type of problem.     The licensee's corrective actions appear to be
                 adequate.
                 This LER is closed.
                 (Closed) LER 327/87-021, Revision 1; An Inoperable Fire Barrier Which Was
                 Not Brought To The Attention Of The SE For One Day, Thus Causing A Viola-
                 tion Of TS On April 17, 1987. Fire door 0-10 in diesel cell 1A-A was
                 found closed, latched and inoperable with a broken self-closing mechanism
                 by an industrial safety individual.       An Assistant Unit Operator (AVO)
                 wrote Work Request (WR)B223640 to repair the fire door on April 16, 1987,
                 but failed to write a fire barrier breaching permit as required by
                 Physical Security Instruction (PHYSI)-13, Fire.      The industrial safety
                 individual researched the issue further and decided a fire barrier
                 breaching permit was required. He informed the SE and a permit was issued
                 and the LCO was entered. The Licensee has counseled the AVO on the
                 requirements of fire barrier breaching permits, PHYSI-13 was revised, and
                 as of Revision 50 it is required that a person must be on an approved list
               - -.         -.       .-                                  -         _
                                                                                                          .--        -      -_
                        .
                                                                        38
                          (Attachment F, Appendix A to PHYSI-13) to hold a breaching cermit. The
                          licensee's actions appear to be adequate.
                          This LER is closed.
                          (Closed) LER 327/87-026, Revision 1; Inadequate Radiological Control
                          Coverage in the Transfer of Radioactive Waste Caused by Personnel Error
                          Resulting in Technical Specification Violation.               This issue involves a                        ;
                          lack of sufficient planning to perform the intended operation per written
                                                                                                                                     '
                          instructions. Radiological Control Instruction (RCI)-13, Access Control
                          of High Radiation Areas Where Radiation Intensity is Greater Than or Equal
                          to 1000 mrem / hour, was in place during the time the incident took place.
                          RCI-13 was issued to cover TS 6.12.2. The licensee has counseled the
                          personnel involved, has instructed management to provide better planning
                          and has revised RCI-13 to better define personnel responsibilities. A
                          review of TS 6.12.2 and RCI-13 indicates that th'e licensee has acted in a
                          responsible manner and the licensee's actions appear to be adequate.
                          This LER is closed.
                          (Closed) LER 327/87-029; Yearly Reporting of Environmental Impact for
                          Plant Design and Operating Changes Not Made Due To A Lack of Proper

'

                          Procedures.         This issue involves a violation of TS 5.3.c (appendix B)
                          which says that the licensee must maintain records of changes in facility
                          design or operation that could af fect an environmental impact.                      Further               >
                          the licensee is to furnish to NRC an annual report containing any                                          ,
                          descriptions, analyses, interpretation, and evaluations of such changes,                                   ;
                                                                                                                                     '
                          tests and experiments. The licensee is required to maintain records of
                          changes in facility design or operation that could affect an environmental
                           impact.    Plant procedures and responsibility requirements were not
                           sufficient to prevent this event.                 The licensee has revised Plant
                          Administrative Instructions (AI)-9 and -19 to require a documented
                           evaluation of changes, tests, and experiments to the facility which could
                           affect the environment as required by TS 5.3.C (Appendix B).                             The
                           chemistry group has completed a study of the facility design and
                           operational changes since September 15, 1984, which could affect the
                           surrounding environs. This study will be included in the next annual
                           report.   The licensee's actions appear to be acceptable.                                                 ;
                           This LER is closed.
                           (Closed) LER 327/87-036; Nonconforming Timing Relays Installed in
                           Containment Air Return Fan Controls Due to Personnel Errors. Containment
                           air return fan 18-B failed to start, per TS acceptance criteria, during
                           the performance of SI-28, Containment Air Return Fans. A modified Agastat
                           relay 7012PH was found to be installed instead of a 7012PF relay.                            A
                           7012PF (120VAC coil) relay was modified using a 7012PH (125 VDC coil)
                           relay as a result of TACFs that were prepared to replace the 7012PH relays
                           with the modified 7012PF relays. The manufacturer states that AC relays
                           cannot be modified by using DC coils to obtain the required relay. The
                            licensee has installed administrative controls to require approval of

j J

 -.w.- _ - - ~- , -. _m                 ---.7   -m.,y-.. , _ . - , m, -    -                ,-   -,,._.,v     , , -     -v,,   .,e .
                           . .     . _-          . . .             .  ..     -   -  -.

.

                                        39
 TACFs by DNE prior _ to implementation.               Agastat 7012PF relays were
 re-installed per Design Change Notice (DCN)-75 by Work Package (WP)-12707.
 The licensee's actions appear to be adequate.
 This LER is closed.
 (Closed) LER 327/87-053; Inadvertent Diesel Generator Start Caused By
 Personnel Inattention To Detail And Lack Of Procedural Clarity During
 Installation Of A Jumper. Diesel generator 18-8 was inadvertently started
 when the terminal screws were loosened to allow installation of a spade
 lug jumper. The procedure, IMI-99-RT6998, Response Time Testing Of
 Engineered Safety Feature Actuation-Safety Injection Signal With Station
 Blackout Units 1 And 2, stated that wires were not to be lifted.              The
 licensee has revised IMI-99-RT699A and IMI-99-RT699B to caution the
 performer to use clip-on jumpers instead of lug type jumpers. Maintenance
 Personnel were counselled on the need to be attentive to details and to
 question unfamiliar procedural steps. The licensee's actions appear to be
 adequate.
 This LER is closed.
 (Closed) LER 327/86-061, Resision 1; Personnel Errors Resulting In Failure
 To Comply With An Action Statement For Limiting Condition for Operation on            '
                                                                                        ,
 the Auxiliary Building Vent Radiation Monitor. The root cause was the
 cancellation of (SI)-470.5, Auxiliary Building Iodine Sampler Flow                     ,
 Estimation, by chemistry personnel in June 1986.               SI-470.5 was to be
 reinstated by December 21, 1986. However, it was not approved until                   :
 December 24, 1986, and not distributed until December 31, 1986, one day               i
 after the auxiliary building vent monitor was declared inoperable and a
  temporary sampler was installed.         The licensee has reissued $1-470.5 and
  this procedure was used from December 31, 1987, until the radiation
 monitor 0-R-90-101 was made operable. The licensee's actions appear to be              ;
 acceptable.                                                                            '
 This LER is closed.
  (Closed) LER 328/87-004; Containment Penetration Did Not Have Redundant
 Over Current Protection Because Of A Personnel Error During Construction.              i
  The cable supplying radiation monitor 2-RI-90-60B (non-safety related) was
  not terminated on the load side of fuse 2-FU2-90-60B. The radiation
 monitor supply cable was connected to the output of circuit breaker 12
 which was the supply side of the fuse. The licensee has corrected the                   !
  problem per work request (WR)-B117832 and verified all of the other                    i
  circuit breaker / fuse combinations for penetrations are correct.             The      i
  licensee's actions appear to be acceptable.
  This LER is closed.
  (Closed) LER 328/86-005; CVI Caused by EMI On A Radiation Monitor.
  Electric Magnetic Interference (EMI) caused the activation of radiation
  monitor 2-RM-90-106 which resulted in a Containment Ventilation Isolation
                                                                                        l
                                                          ___________ _ _ _ - .

.

                                    40
 (CVI). No actual high radiation levels were found. The source of EMI was
 not identified; however, some heli-arc welding.had taken place and it was
 surmised that welding was the cause. The licensee initiated Design Change
 Notice (DCM)-2276 to add capacitors to several radiation monitors to
 reduce EMI induced actuation. At the present time the licensee has stated
 that an ECN will be issued about the first of May and implemented by June.
 This DCN is currently in the licensce's TROI system for completion. The
 licensee's corrective action appears to be adequate.
 This LER is closed.
 (0 pen) LER 328/87-05; Train B Containment Ventilation Isolation Caused By
 An Unknown Source.      This item irvolved an inadvertent containment
 ventilation isolation (CVI) which occurred on March 5,                         1987. This CVI
 resulted from spurious signals from the channel containing Radiation
 Monitor RM-90-106. After Analysis of the event, the licensee was unable to
 determine a root cause. Therefore, the only corrective actions taken were
 to clear the CVI and return the radiation monitor and its associated
 isolation valves to normal service. During review of this LER, the
 inspector reviewed four additional CVIs which have occurred on (LER
 328/87-008 RI) November 27, 1987, (LER 328/87-009) December 5, 1987, and
 (LER 328/87-010) December 21, 1987. All of these CVIs are associated with
 the channel containing RM-90-106, and root cause has not yet been
 determined for any of the listed events.     This item remains open pending
 determination of root cause and completion of corrective action for all of
 the above listed events.
 (Closed) LER 327/87-059; Alpha Contamination Checks Not Performed As
 Required Due to Inadequate Accountability for A Surveillance Requirement.
 This issue involved Alpha Contamination Checks not being performed on two
 sealed sources (283N and 662N) as required by TS Surveillance Requirement
 4.7.10.2.b and Surveillance Instruction 51-56, "Byproduct Material
 Inventory and Sealed Source Leak Test." The licensee has determ'ned rcot
 cause to be an inadvertently misfiled inventory card (283N) and less than
 adequate accountability for the performance of the surveillances. The two
 sources were checked for contamination and no detectable leakage was
 identified. An inventory of known byproduct material was completed and a
 survey of plant supervision was conducted to identify any other additional
 sealed sources which may have been missed. These actions are documented
 via TVA memo dated October 26, 1987, (RIMS S53-871026-863). Appropriate
 plant personnel were reminded of the importance of controlling byproduct
 material via TVA memo dated, October 22, 1987, RIMS S53-871022-837.                         In
 addition, in order to provide adequate accountability, responsibility for
 51-56 is being transferred to the Radiological Control section. This
 transfer will be completed by March 1, 1988, and is being tracked by
 Corporate Commitment Tracking System control number NC0-87-0291-003.
 These actions taken by the licensee appear to be acceptable.
 This LER is closed.
                                                                                                _________ - ___
  -   . . -                -   .       ..         _ -
                                                                                                            i
                                                                                                             ,
    =
              .
                                                       41                                                    l
                                                                                                            1
               (Closed) LER 327/86-010; Diesel Generator Start from Inadvertent Removal
               of Fuse. During a fuse check the fuse was dislodged, de-energizing the
               ED1 emergency start circuit, and starting the diesel generator.                The
                licensee has added a caution staterant to the appropriate sections of
               50182.2, Manual Rolling and Starting / Synchronizing Diesel Generator.
               This LER is closed.
                (Closed) LER 327/87-033; Adequate Design Calculation are Unavailable for
                the 125 VDC Vital Battery V Causing Potential Degrading of the System.
               This issue involved potential problems on the Sequoyah 125 volt direct
                current (VDC) vital battery V. These problems have been identified on a
                TVA significant condition report (SCR) SQNEEB8746 which is used by
                division of nuclear engineering (DNE) to identify problem type issues.
                These potential problems are due to the inabi.lity of the license to
                produce adequate design calculations to support the plant design bases.                     ,
                                                                                                            '
                DNE, electrical engineering branch (EEB) has established a minimum set of                   '
                essential calculations to support the design bases of Sequoyah nuclear
                plant. These calculations are specified in procedure method (PM) 86-02.
                Hold order 1606 on site operation instruction (501)-250.5,125 Volt DC
                Battery Board No. V, will be in effect until the deficiencies associated                    ;
                with vital battery V have been resolved. The licensee's actions appear to
                be adequate.                          -                                                     .
                This LER is closed.
                (Closed) LER 327/86-025: Two Inadvertent Diesel Generator Starts During
                Walkdown Activities. During a fuse identification check a control fuse
                was pulled. When the fuse was replaced the normal feeder breaker to the
                28-B, 6.9 KV shutdown board tripped and the board transferred to the
                alternate power supply. Personnel attempted to transfer back to the
                normal supply without verifying the board deenergized, causing the diesel
                generator to start.       Investigation revealed a component failure in the
                 surge protection circuit.     The component was replaced.
                A second inadvertent start occurred during removal of a panel from battery
                board I for breaker name plate verification. The panel slipped and
                tripped a breaker which caused a loss of voltage signal, starting the
                                                                                                             I
                diesel generator. Additional personnel were used to assist in removal of
                the pinels to support the weight. A design change to add handles to the
                panels had been cancelled due to the low frequency of panel removal. This

4

                design change is being reevaluated by the licensee.                The licensee's
                actions in both diesel generator starts appears to be adequate.
                This LER is closed.
                 (Closed LER 327/86-022; Inadvertent Containmen+. Ventilation Isolation
                 (rJ/I) Caused by Radiation Monitor (RM) Spikes. On May 15, 1986, two CVIs

.

                cccurred, on Unit 1 the CVI has been determined to be caused by Electric
                Magnetic Interference (EMI) generated by low flow /high vacuum alarm switch
                 chatter on 1-RM-90-131 during purging initiation.              On Unit 2 the CVI
l
            .   ,,-,                          - .        - , , -     .- .-- - .        -        - . - . - -
  __ _ __   --_       __         __ .   .                                        -         _ _
          .
                                                   42
             occurred due to personnel error when an operator deenergized 2-RM-90-106
             to prevent initiation due to EMI generated by welding. The licensee has
              submitted DCR2276 to add EMI suppression circuitry to the RMs (IRM90 106
             and 131, 2RM90-106 and 131). The DCR is being tracked by the licensee's
             commitment tracking system and has a completion due date of May 1,1988.
             Additional corrective action consisted of counselling the personnel
              involved in the Unit 2 CVI and issuing a training letter to all licensed
              personnel and STAS, dated June 25, 1986.
,
,
              This LER is closed.
!             (Closed) LER 327/86-045; Fuse Short During Maintenance on ERCW Valve
'
              Caused Diesel Generator to Start. The cause of this event was personnel
              error. However, underlying the cause is a fuse coordination problem and a
              quality problem with the Bussmann MIS-5 fuses used to replace the KAZ
              actuators.      Bussmann has indicated a potential design defect with the
              MIS-5 fuses and provided TVA with a method of testing to verify fuse
              operability. TVA committed to replacing all defective fuses (MIS-5) prior
               to restart. LER 87-030 has documented that Bussmann MIS-5 fuses have been
                replaced with Littlefuse FLAS-5 fuses. Discussions with the TVA personnel      i
                indicated all fuses have been replaced per ECN 6854.
              The fuse coordination problem is caused by using the same size fuses for         i
               both feeder and branch circuits, rather than coordinating the fuse rating
                to smaller sizes nearest the load.      TVA has committed to review all
                circuits for similar coordination problems prior to Unit 2 restart and to
                implement certain modifications after Unit 2 restart per the LER. The
                fuse coordination issue is being tracked as IFI 327,328/86-57-01.
                This issue is closed.
                (Closed) LER 327/86-049; Diesel Generator Start on Loss of 6.9 KV Shutdown
                Board Voltage Due to Personnel Error.      Following maintenance, during

'

                restoration of electric system line up, an operator opened the wrong
                breaker (normal feeder breaker to the 18-B 6.9 KV shutdown board) causing      -
                the diesel generators to start. The event was discussed with the operator      ;
                and signs were added to the 6.9 KV unit boards to clearly identify them.

>

                This item is closed.
                (Closed) LER 327/87-051; Skid Mounted Valves Were Not Checked Every 31
                Days.    Technical Specifications (TSs) 4.7.3.a, Ccmponent Coo'ing Water
                System (CCS) and 4.7.4.a, Essential Raw Cooling Water (ERCW) System,
:               requires valve position verification every 31 days for valves servicing
                safety related equipment.       The licensee's Department of Nuclear
                Engineering (DNE) has identified all safety-related vendor supplied skid
                mounted equipment. Surveillance Instructions for CCS (SI-32) and ERCW          i
                (SI-33.1) were revised, revision 19 and 10 respectively, to add the skid        !
                mounted valves to the 31 day surveillance verification.The adequacy rf the

,

                control room drawings is being followed under Violation 327, 328/87 -01.

' <

                                                                                               l

.

                                     43
This issue is closed.
 (Closed) LER 327/86-042; Two Surveillance Requirements Not Performed
 Because of Inadequate Procedures. This issue involved: (1) several
 safety related pumps not being tested in accordance with 1977 ASME Boiler
 and Pressure Vessel Code, Section XI, Subsection IWP3110; and (2) the
 calibration     of temperature sensors, thermocouples and resistance
 temperature detectors not being performed as required by TSs. All actions
 associated with this issue have previously been reviewed and determined
 acceptable in Inspection Report 327,328/87-36 with the exception of the
 licensee's Request for Relief from the above referenced ASME Section XI
 requirements. On October 23, 1987, the NRC Office of Special Projects
 issued a lettee and safety evaluation granting the Relief requested.
 Therefore, all required actions pertaining to this issue are complete.
 This LER is closed.
 (Closed) LER 327/87-056; Combined Bypass Leakage Limit Was Potentially
 Violated Due to An Inadequate TS and Lack of a Specific Design Criteria.
 During a aesign review it was determined that 26 penetrations to the
 containment were not included in table 3.6-1 of the TS. The licensee has
 concluded, based on review of SI-158.1, Containment Isolation Valve Leak
 Rate Test, which included all but two of the subject valves, that a high
 degree of confidence exists that no violation of TS occurred.        The 26
 valves identified have been added to the SI-158.1 calculation for
  irclusion in the requirements of TS 3.6.1.2.c.    The licensee has submitted
 a change to TS to include the above valves to Table 3.6.1, Secondary
 Containment Bypass Leakage Paths of TS. The TS change request (number
 TVA-SQN-TS87-33, dated September 17, 1987) changes Table 3.6.1 and defines
 "Bypass Leakage Paths to The Auxiliary Building".      SI-158.1 is scheduled
  for completion prior to Unit 2 restart.
 This LER is closed.
 (Closed) LER 327/87-060; Inadvertent Start of Diesel Generator Caused By
  Inadequate Procedure During Shutdown Board Maintenance. While removing a
  tee wrap from wiring bundles an operator inadvertently shorted c-lectrical
  studs in the board causing a diesel generator start.      In the process of
  shutting down the diesel generator the 1A-A EDG tripped on overspeed.
  Special Maintenance Instructions SMI-1-202-3/4 were revised to cover the     ,
 exposed electrical studs and to inhibit the start signal by placing a test    i
                            Investigation of the overspeed trip revealed RTV
                                                                                '
  switch, 43TC, in test.
  in the oil passage of the governor hydraulic actuator. The RTV had been
  applied to the electrical connectors to the actuator in an attempt to seal
  the cables against hydraulic oil intrusion. The actuators on all diesel
  generator governors were replaced and a caution sign placed near the
  governors that prohibits the use of RTV on the actuator.
  This LER is closed.
  __ _ _    _
              .
                                                   44
                (Closed) LER 327/86-41; Two Diesel Generator (DG) Starts Caused By A
                Personnel Error and Procedure Inadequacy During Fuse Replacement. On
               September 14, 1986, while replacing KAZ actuators, an inadvertent EDG
                start occurred when power was removed from the start logic relay panel.
               During this event a high temperature trip of the IB-B EDG was actuated.
               The root cause of the inadvertent EDG start was the improper marking of
                the Main Control Room (MCR) drawing following a modification. The
               modification was properly documented on the Unit 2 drawings, but not on       <
                the Unit 1 drawings.      The licensee's corrective action included the      '
                training of personnel on proper markup procedures, combining MCR common
                equipment drawings, and revising the procedure used for MCR temporary
                drawing changes. The high temperature trip of EDG 1B-B was determined to
                be caused by a misaligned cooling water valve lineup.         The licensee's
                corrective action included issuing a training letter to all Unit Operators
                (U0s) and above, detailing procedures for removing EDG cooling water
                supply from service and verifying with the manufacturer that no damage
                occurred to the EDG.
                The second EDG start occurred on September 17, 1986, while removing KAZ
                type fuses. An operator inadvertently pulled a power supply fuse for the
                EDG control emergency start circuit. The licensee's corrective action        i
                consisted of replacing the fuse and cautioning the operator. A review of
                the above corrective actions and discussions with licensee personnel
                indicate that actions accomplished are adequate to close this LER.
                This LER is closed.
4
                (Closed) LER 327/87-062; Unplanned Loss of Manhole 7B Missile Protection
                for B Train Diesel Generator Cables Due to Programmatic Deficiency in The
                Design Change Process. During the work process to install a modification
                 it was determined that missile protection for manhole 78, containing the
                Units 1 and 2 B train cables, was not maintained. The cause of this event
                has been determined to be a failure to properly identify manhole 7B as
                missile protection during the design change process, compounded by a
                 failure of the approval and review process to adequately evaluate the
                effect of the construction activity on the plant operability status. As a
                result of this event both trains of diesel generators were inoperable at
                 the same time. The A train EDGs were inoperable for other reasons at the
                time. It is noted that only missile protection was lost for the B train
                and in the event the diesel generators were required for power they would
                have functioned as designed. The inspector reviewed the report and
                determined that the event had been adequately resolved. The
                 recommendations provided in the report, when properly implemented, will
                 limit the probability for recurrence of this type event.
                 This LER is closed.
         9.      Event Followup (93702, 62703)
                 a.    On December 1,   1987, maintenance was being performed on motor
                       operated gag valve 2-MOV-87-23B, the gagging device for Upper Head

.) 1

 - __    _-.          . . . .   --.                           .    .                    ..
   -
         .
                                                45
               Injection flow control valve 2-FCV-87-23A. Part of this maintenance
                                    .
               activity required that the gag motor rotation be checked.           This
               required that the gag valve be placed in the mid-position and the gag
               motor hand switch be placed in the open position to verify proper
               stem rotation. When the unit operator was requested to open the gag
               valve the operator went to open on the hydraulic operated valve
               2-FCV-87-23A. The valve opened and resulted in mechanical damage to
               the gagging device. FCV-87-23A should not have opened with the gag
               valve in the mid position.       The hydraulic valve is interlocked with
               the gag valve such that it should only open when the gag valve is
               fully raised (open). The gag valve shut indicating light was also
               burned out such that the gag valve did not indicate that it was in
               the mid position.        The licensee is still investigating why the
               hydraulic valve opened when the gag valve was in the mid position.
               The root cause of this event included poor communication and equip-
               ment malfunction. The licensee responded with prompt corrective
               action and in addition established a root cause analysis task force.
               Because of the licensee's corrective action, and because there was no
               material damage to the cperability of the system or failure to
                implement procedures, a violation will not be issued.
                                                                                              !
            b. On November 25, 1987, during maintenance on the Unit 2 Auxiliary               ;
               Feedwater system (fit up check of the fire main supply spool piece),           f

4

               three to five gallons of water spilled from a blank flange which was

j removed. This maintenance was being performed within the boundaries 1 established by a work authorization clearance. The source of the

               water was from a section of piping within the clearance boundary that          ,
               was not adequately drained or depressurized during establishment of            !
                the clearance. Unrelated to the spool piece maintenance, but
               occurring simultaneously, Surveillance Instruction SI-247.1008,
                Response Time Testing of the Engineered Safety Features Actuations,
               caused the "A" SG level control valve (2-LCV-171) to cpen releasing
                the water trapped between the level control valve and the spool piece
               maintenance boundary valve. Three to five gallons of water flowed by
               gravity out of the spool piece flange.
                TS 6.8.1 requires that written procedures be established, implemented
                and maintained covering the referenced activities.
               Administrative procedure, AI-3, section 4.2.5 states, "The SE shall
                verify that pressure is zero and equipment drained prior to issuing a
                mechanical clearance."
                Contrary to the above, the licensee failed to adequately drain and             l
                depressurize the portion of the system isolated to support the                 I
                maintenance activity.       This is considered a second example of VIO
                327,328/87-76-02, which is addressed in paragraph 6 of this report.
                This item was determined not to meet the requirements for a licensee
                 identified item because it was event identified and it was the direct         i
                result of a failure to adequately implement a procedura.                       l

4 '

                                                                                               l

'

                                                                                               1
      .-                      _       -                              _
                                                                       _     __ _,         _~
 .
                                     46
  c.   On July 1,1987, the IA-A EDG failed to mect acceptable speed and
       voltage parameters (56Hz vs 58.8 required). Swings on load reject
       reached 7960, while the maximum allowed was 7656. PRO 1-87-217 and
       SQP'871238 described the failure of SI-26.1A. The CAQR stated that
       the voltage regulator stability settings should be optimized to

,

       minimize overshooting, and that the IA-A EDG did not meet Regulatory
       Guide 1.9 requirements. The CAQR determination was that the voltage
       regulators are overdamped (i.e., response time reduced beyond
       nominal).
       CAQR SQP871238 was evaluated by P0RS. It determined the affected EDG
       to be operable and the failed SI not a reportable event based en an
       evaluation that the voltage necessary to cause overcurrent relays on
       safety equipment to trip is approximately 8800 volts. The tolta.ge
       observed during the test was 7960 volts and that previous runs of
       SI-26 had been run without incident. The licensee determined that
       the "intent" of R.G.1.9 had been met in that the voltage required to
       cause over current was not reached.
       On October 14, SI-26.2A was run on 2A-A EDG,      It failed to meet the
       acceptable voltage of 5520 volts minimum prior to output breaker
       closure, but the breaker closed at 5200 volts. The breaker is
       interlocked to prevent closure until voltage is above 5520 volts, and
       the speed is above 850 rpm.     Troubleshooting on October 21, found a
       voltage regulator printed circuit card diode installed backwards.
       PRO 2-87-94, written on October 27, identified a diode in the voltage
       regulator as being installed backward, causing the improper response
       of the vcitage regulator (according to LER 327/87-70).            This
       particular voltage regulator was installed by the licensee on
       November 8, 1986, in response to WR B208401, in order to troubleshoot
       the cause of reported voltage fluctuations on the 2A-A EDG.
       Post-maintenance testing only required that SI-7 be run to verify
       that the 2A-A EDG was operable. This test is inadequate to verify       l
       proper operation of the voltage regulator in that it does not test
       operation of the voltage regulator under rapid loading / rejection
       conditions. As a result of the inadequate post maintenance test, the
       defective voltage regulator was not discovered until the 16 month       i
        surveillance (SI-26.2A) was run in October 1987.                       l
                                                                               ,
        LER S7-70 was written on part 21 (as-found date is October 21). PRO
       2-87-94, written on October 27, 1987, documents the troubleshooting
        findings of the maintenance workers who discovered the innproperly
        installed diode. The LER states that the cause of the early closure
        is still under investigati:n.     The use of an inadequate test is a
       violation of ths TS 6.8.1 reouirement to establish, implement, and
       maintain written procedures covering the plant activities including
        surveillance and test activities of safety related equipment. This
        item is identified as VIO 327,328/87-76-01.                            I
                                                                                I
     S
                                                                               l
                                                                               !
                                                                               !
                                                                               !

=

     .
                                          47
 10.  Part 21 Reports
      (Closed) 327,328/P2184-04, Incore and Excore Neutron Monitoring Fittings.
      This item was addressed in IE Information Notice 84-55. This item was
      also reviewed as part of the Sequoyah flux thimble guide tube ejection
      eve-     The inspector reviewed the licensee's action with respect to IE
      No'      .4-55 and found it to be acceptable.
      This item is closed.
 11.   Licensee Actions on Previously Identified Inspection Finding (92701)
       Inspector Followup Items (IFIs) are matters of concern to the inspector
      which are documented and tracked in inspection reports to allow further
       review and evaluation by the inspector. The following IFIs have been
       reviewed and evaluated by tne inspector.       The inspector has either
       resolved the concern identified, determined that the licensee has per-
       formed adequately in the area, and/or determined that actions taken by the
       licensee have resolved the concern.
       (Closed) IFI 327,328/86-31-04; Review of An Inadvertent Control Room
       Isolation Following Completion of Licensee Investigation. This event was
       reported to the NRC in LER 327/86-022, Inadvertent Containment Ventilation
       Isolation (CVI) Caused by Radiation Monitor (RM) Spikes. This LER was
       reviewed and closed elsewhere in this report.
       This item is closed.
       (Closed) IFI 327/84-11-03; Flux Thimble Guide Tube Incident Review. This
       item was the original tracking item for the flux thimble guide tube        ,
       incident. Subsequent to this identified item, IR 327,328/84-24 provided    1
       additional review of the incident and three violations were issued. The
       violations were closed in IR 327,328/85-27 and later reopened in IR 327,
       328/87-43 due to concern for the adequacy of the root cause determination
       and the corrective actions. This IFI was reopened along with all other     1
       items associated with the incident in order to ensure that a clear         )
       auditable closure existed.                                                 '
       The relevant issues will be tracked by the final resolution of the
       violations issued in IR 327,328/84-24.
       This item is closed.
                                                                                   l
       (Closed) IFI 327/84-20-02; Verify That Detailed Procedures Have Been        l
       Established and Are Being Used. This issue involves the July 9, 1984
       disassembly and repair of the B-B Auxiliary Air Compressor (AAC), which is
       part of the saf9ty-related system auxiliary control air.   The disassembly
       and repair were accomplished using a maintenance request (i.e. , without
       detailed procedures). TS 6. 8.1. requires that written procedures be
       established, implemented and maintained covering activities referenced in
       Appendix A of Regulatory Guide 1.32, Revision 2, February 1978. Paragraph
       9 of Appendix A, Procedures f or performing maintenance, requires that
       maintenance which can affect the performance of safety-related equipment
                                                                                  1
                                                                                  j
                                             i
 =
   ,
                                        48
     should be properly preplanned and performed in accordance with written
     procedures.
     The inspector has contacted mechanical maintenance and received verbal
     conformation that the maintenance of safety-related equipent is being
     scheduled and approved procedures are being used. Maintenance instruction
     (M1)-10.36, Auxiliary Air Compressor Rebuild, has been reviewed and
     appears adequate. A review of corporate commitmer.t tracking system (CCTS)
     #dC0085-0491-019 ider,+.ified seventeen Critical Systems, Structures and
     Components (CSSC) corepone.1ts that required mis. All seventeen mis had
     been prepared and cpproved prior to October 1986. The licensee's action
     appears to adequate.
     This item is closed.
     (Closed) IFI 327,328/86-60-07, Generic Fittings. This issue was included
     in the licensee's program for the control of mixed compression fittings in
     safety-related applications. Due to an omission, this item was not closed
     when the other outstanding generic fittings issues were closed in IR
     327,328/87-65. The closure statement in 327,328/87-65, is also relevant
     to this item.
     This item is closed.
     (Closed) IFI 327,328/86-69-01; Diesel Generator Starting Air System
     Discrepancies.   During : walkdown of the diesel generator start'ng air
     system the inspector identified numerous apparent . discrepancies between
     drawing number 47W839-1, the System Operating Instruction (S07)-82.1F,
     Starting Air System for Diesel Generator 1A-A, and the system 'as-built
     configuration.    The inspector evaluated the licensee's response to 16
     apparent discrepancies and 2 questions. The licensee responded adequately

i to the inspector's questions and no further issues were raised. The

      inspector verified the cvrective actiori in each discrepancy through
     direct inspection.    The items have been corrected in the procedures, in
     the field, and thrnugh red-line c0rrections to the control room primary
     drawings. Drawing Deviation forms exist to assure permanent drawing
     updates will be implemented.       The licensee's corrective action is
     adequate.
     This item is closed.
      (Closed) IFI 327,328/86-28-18; Sof tware Security in the SPDS Computer
      System. During the review of the Safety Parameter Display System (SPDS),
      the inspector expressed concern that access to the sof tware programs
      should be further controlled.       Since that time the licensee has
      implemented the following controls to guard against software security
      problems:
      -
            The source code (langusge thet it. used to build / modify programs) was
            removed frem the Tectnical Support Center (TSC) SPDS computer. The
    .-                      _
                                     - .       .----      .  .- -       _
                                                                                             .. .   -     . - .    -                -
                                                                                                                                              ~ ..
                                                                                                                                                   e
    -.                    ,
                                                                  49

< .

                                                                                                                                                   !

'

                                   code was placed on magnetic tape held under administrative control by
                                   Sequoyah Instrtmentation Maintenance section,                                                                   i
                           -
                                   Password protection was provided to the TSC/SPDS Computer system.                                               -
                           -
                                   A keycard is required to access the computer.
                           -
                                   Restricted access was established to the computer room.
                           -
                                   Modifications of the TSC/SPDS software shall be in accordance with
                                   Sequoyah procedure SQE-13, Software Configuration Control, Re'. 4,
                                   and.SQA-193, Quality Assurance for Computer Software Systems, Rev. 1.
                           Adequate measures appear to have been taken to protect against software
                            security problems.
                            This item is closed.
                            (Closed) IFI 327/87-11-07; Verification of Corrective Actions for Element                                              i
                            Reports CO 11103 - SQN Rev. 5 and CO 11203 - SQN Rev. 3. The inspector                                                 *

'

                           determined that the specific concerns addressed in this IFI were addressed
                            by the safety evaluation report (SER) to be completed by NRC. This item
                            is redundant to that closure process. Therefore, this IFI is closed and
                            the resolution of these element report issues will be addressed by the                                                 ,
                            issuance of the NRC SER on CO 11301 - SQN Rey, 3.                                                                      !
                                                                                                                                                   ;
                            This IFI is closed,

i

                            (0 pen) Inspector Followup Item 327,328/86-69-05, Backup Power Supply For

, The Emergency Notification System (ENS). IE bulletin 80-15 required  ; '

                            determination and verification of the status of the backup power supply to                                             ,
the ENS system. This IE bulletin, is;ued June 18, 1980, required a

'

                            verification that the ENS telephone be conne:ted to a supply of power that

. '

                            would remain operable upon a loss of site power. The bulletin required                                                 _
'
                            that facilities without a redundent supply make necessary modifications
                            and provide such a connection.         TVA responded to the NRC in letters,

.

                            L. M. Mills /TVA .o J. P. O'Reilly, August 29, 1980, and J. L. Cross /TVA to
                            J. P. 9'Reilly, September 5, 1980, and indicated that a Design Change

j Request had been submitted and that testing would be accomplished when the

modification was complete. TVA sent a followup letter, L. M. Mills /TVA to -
J. P. O'Reily, March 3,1981, indicating the modification was expected to

i be complete at Sequoyan by April 21, 1981. Between March 1981 and i'

                            November 1986 (almost 6 years), Sequoyah records and licensing could
                              locate no correspondence to indicate followup on this item. TVA letter                                               l
                             R. Gridley/TVA to J. Nelson Grace, November 5, 1986, referenced an
                                                                                                                                                   ~

'

                            August 27, 1986 telephone call between TVA and R. Priebe/NRC which

4

                              indicated that the item need not be resolved before startup, provided a
                              schedule was being developed to correct the problem. The TVA letter
indicated that the design work would be completed by February 1987, and
                              that testing would be completed within four weeks once startup issues no

1

                              longer dictate the schedule. TVA letter R. Gridley/TVA to USNRC document

r

                                                                                                                                                   i

f

  ,  _ ~ _ . . _ . . , _ _ _ , , _       - , ,  , _ _ . _     ,,          , . , _ _ _ . _ _ _ _   _
                                                                                                      _ ,      _ _   . . , , _ _ . _ _ , , ,,
  _-       -
     .
       ..
                                            50

'

       control desk, May 15 1987, noted that TVA has been unable to meet the
        February commitment due to allocation of resources to startup items. The
        letter indicated a new schedule for design completion by the end of
       January 1988.      Modification completion (including required testing) was

-

       not addressed in the letter.
        The inspector discussed this item with communications personnel, Nuclear
        Engineering Branch personnel and' licensing personnel in an attempt to
        determine if a schedule existed for the rodification (start to comple-
        tion). No schedule was located. The inspector concluded that this . item
is a long-term outstanding bulletin requirement that has not been

-

        implemented in a timely manner.      Lack of documentation and rotation of
        personnel involved, added difficulty in assessing the cause of the delays.
        This item will remain open pending further investigation and corrective
        action by TVA. This is not a startup item and this item is being reviewed for
        shutdown plant consideration pending licensee corrective action.
        (Closed) IFI 328/81-12-01; No Pl2nned Testing To Verify The Operation Of
        Each Of The PORV Motor Operated Block Valves During A Blowdown Of Pres-
        surizer Pressure Using The PORV At Normal Operating Temperature And
        Pressure.     TS 3-4.3.2 requires that the power operated relief valves
        (PORVs) be stroked every 18 months and the blocking valves are to be

, cycled full stroke every 92 days with the PORVs closed (the block. valves

        are not cycled against differential pressure). This is done to verify the
operability of the overpressure protection system. The PORVs and blocking

! valves are stroked per SI-166.40 once very 18 months. The blocking valves , are cycled open per SI-116.1.1 once every 92 days. The inspector was not

able to identify a legal requirement or a licensee commitment intended to

! cycle the blocking valves against normal RCS operating temperature and l pressure (blowdown). The licensee has decided to forego testing of the i

        blocking valves against temperature and pressure (blowdown) for the
        following reasons:

4 4

              -
                    The valves were purchased from the vendor with the requireaent
that they operate during operating temperatures and pressures.
                    The licensee expects these valves to operate under the condi-
'
                    tions for which they were designed.

i !

              -
                    The licensee does not wish to breach the primary pressure
i                   boundary at normal operating temperature and pressure without
                    adequate justification.
'
        The licensee's actions appear to be adequate, this item is closed.

' b (Closed) Item 327-328/S6-17-04; Pre-startup Training Commitments. This , issue involved a letter from NRC rerion II to TVA subject: NRC inspection , report 50-327,328/86-17 and accepM/g the TVA commitments as stated in

TVA's respnnse to the inspectie, report oated May 28, 1986. The

j- commitments are as follows: l

:
;
                                                          .
 o     .
                                             51
         -
               By startap, all operators will be provided with a training letter on
               major plant modifications completed during the extended outage.
         -
               By Unit 1 startup, the Unit I operators will be provided with a
               training letter regarding precautions to be taken on a unit startup
               with high boron concentration and potential positive moderator
               temperature coefficient.
         -
               By Unit 2 startup TVA will provide additional startup simulator
               training for licensed employees who will be involved in the Unit 2
               startup.
         A review of the Corporate Commitment Tracking System (CCTS) indicates that
         the above mentioned items were committed to in the CCTS. The items
         required for Unit 2 restart are completed or are being tracked by CCTS.
         Those items required for unit I restart are being tracked by CCTS.       The
          licensees actions appear to be adequate.
         This item is closed.
         (Closed) IFI 327,328/86-46-04; RHR Pump Vent Arrangement. This issue
          involved the post-LOCA swapover of the RHR pumps to the containment
          recirculation sump from the refueling water storage tank. The pumps are
         vulnerable to loss of pump suction due to air or steam binding if the pump
          swapover is not timed appropriately. This issue was discussed with Office
         of Special Projects, Projects Division management (A. Marinos, E. McKenna)
          the weet af January 5,1988. It was determined that the swapover concerns
         were c-     71c to plants that did not have automatic swapover features on
          the RHR pumps. Sequoyah has automatic swapover of the RHR pumps based on
          refueling water storage tank and containment recirculation sump permissive
          switches and is not subject to this specific concern. Office of Specia)
          Project memo (A. Marino/ K. Barr) dated January 20, 1988, confirms that
          the concern is not specific to Sequoyah.       The generic issue is being
          forwarded to NRR for review.

'

          This item is closed.
   12. Design Change Prc ess Waivers (37700)
          To correct past problems in the design change process TVA committed in
          section II.3.0 of the Sequoyah Nuclear Performance Plan to implement a
          transitional design change program prior to restart, and a final program
          after restart.    Two previous inspections documented in inspection reports
          327,328/87-42 and 327,328/86-63, found the transitional design change
          program to be acceptable.
          During the change from the old methed of processing engineering change
          notices (ECNs) to the transitional design change program, a number of
          waivers were granted to allow completion of in process ECNs under the old
          program.    The old program was covered by Administrative Instruction
          SQEP-AI-11, Handling of ECNs. SQEP-13, Procedure for Transitional Design
                                                                                                             i
                                                                                -
                                                                                   , _ _ _ _ _ _ _ _ _ _ ___
           .     . _ _ . .   . _ _ _    . -  -    --    .           .       .       - .    .   . .
         .
                                                     52
                                                                                                          t

e , Control, covered the transitional program. Unitized ECNs and Configura-  !

           tion Control Drawings (CCDs) were required under the transitional program.                      ,

'

          The Project Engineer was required to approve waivers to the transitional                        !
           program, which were usually granted ia order to keep some work activities
           ongoing. For example, waivers were granted to allow use of the existing

'

          drawings when CCOs did not exist. A total of 90 ECNs were processed using                       i
          waivers. The usage of waivers was stopped in March 1987. Revision 5 of

.

           SQEP-13, Ssued in July 1987, removed the allowance for the Project
Engineer to grant vaivers to allow performance of modification design work j
           under SQED-AI-11.

'

           In order to document that adequate design control was maintained for those                     ;

>

           ECNs worked as a waiver to SQEP-13, a verification checklist was included
           in each ECH pekage. Each checklist is signed by the preparer, a
           reviewer, the principal engineer, and the lead engineer. The checklist
verifies the following six items:  ;
                    -
                           Appropriate design criteria / design input requirements have been
                           reviewed including the restart design basis document.
                    -
                           Appropriate configuration control drawings or the latest
                           revision to the as-constructed drawings were reviewed and
                           approved as input for design.
-
                           All previously approved field change requests (FCRs) that are
:                          not yet incorporated into design drawing / documents were reviewed
and effects of these FCRs were accounted for in design, t

a  ; i -

                           All previously designed but unimplemented ECNs were reviewed,
;                          and effects of these ECNs were considered in design.
                    -
                           Any outstanding L-Design Change Requests (DCRs) were reviewed
                           and the effects of these L-DCRs were included in design.                       i

! -

                           All existing Temporary Alteration Control Forms in affer.ted area
l                          were reviewed and determined not to affect the desigra.
            The inspector reviewed four ECNs (L6828, L6844, L6886, L6888) that had
.           been processed using waivers. ECNs L6844 and L6888 contained the

j completed checklist in the ECN package and the other two did not. For ECN

            L6844 the checklist was added as revision one to the ECN package. For ECN
            L6888 the checklist was part of the original ECN revision zero. With the
            completion of the checklist review and incorporating the checklist into
            the ECN package, the review of ECNs processed with waivers will be
            adequately documented to indicate that design control was maintained.
 l
            Discussions with engineering personnel indicated that the review for the
            checklist was time consuming but no conditions adverse to quality had been
             identified. Also, the inspector reviewed two computer printouts listing                       ,

',

            all the CAQRs concerning ECNs and none relating to the waiver process were                     I
             found,                                                                                        j
                                                                                                           l

e I

                                                                                                           I
                                                                                                           i
   - . -                             ,.        ..         -_ -- - -     __.   _ _ -
                                                                                        - _ _ - - -. . . l
  -- _ . .     _           _     _  _                                   .-    __         __
           =
                 .
                                                        53
                                                                                                       .
                   The inspector reviewed two audits conducted by the engineering assurance

'

                   (EA) oversight review group over the Design Baseline Verification Program           l
                   (OBVP). The first audit (EA-0R-001) was completed April 27, 1987. For the           l
                   transitional design change control program two action items (0-09 and               !
                   Q-11) were identified. A supplemental report (EA-0R-001-5) was completed
,
                   September 28, 1987. Q-09 contained recommendations for such items as
                   various additional signoff requirements in the ECN review process, and
                   identifying who approves ECNs. EA concluded that the recommendations were
                   implemented in revision 5 to SQEP-13 issued July 7,1987, and considered
                   this item closed.        Q-11 concerned the usage of waivers to bypass
                   implementation of SQEP-13.      The waivers were stopped in March 1987, and
                   revision 5 to the procedure removed the waiver clause.            The EA team
                   considered the SQEP-13 implementation using waivers closed.
                   In conclusion, the inspector found that the usage of ECN waivers har
                   stopped. ECNs that were processed using waivers are receiving ar, addi-             ,
                   tional review using a checklist to verify that adequate desigi control was          i
                   maintained. These reviews are being adequately documented as part of the            i
                   ECN package and no quality concerns have been identified.
                                                                                                       ,
                   This issue is closed.
             13.   Cold Overpressure Protection Review (TI 2500/19)
                   Temporary Instruction 2500/19. "Inspection Of Licensee's Actions Taken To
                   Implement Unresolved Safety Issue (USI) A-26: Reactor Vessel Pressure               '
                   Transient Protection For Pressurized Water Reactors".
                   In order to verify the acceptability of the licensee resolution of USI              -
                   A-26, the inspector, using the guidance of TI 2500/19, reviewed licensee
generated documents described below. All of the items requiring verifi-
                   cation are not addressed in this report. However, several items have been
                   verified and a number of items requiring further staff review and/or
resolution are identified below.

'

                   Compliance With Technical Specification Requirements

. i _ There is currently no TS pertaining to the Reactor Coolant System (RCS) i

                   Cold Overpressurization Hitigation System (COMS). Therefore, there are no
                    limiting conditions for operation or surveillance requirements for COMS as
                   a system.       However, testing of various components within the system is         i

'

                   being performed and is discussed below.            Testing may not be all           '
                    encompassing, however. Subsequent to conversations between licensee                ,
                    personnel and NRC staff, the licensee has agreed to initiate, and submit
                    for NRC review, a TS for COMS. The licensee's position, however, is that
                    this need not be accomplished prior to restart of Unit 2.         This position
                    is currently being reviewed by NRC-0SP-Headquarters.                               i

u

.

! ! ..- , . - -- - --

 .
                                                      54
                                                                                                          ,
   System Redundancy and Independence                                                                     ,
                                                                                                          '
   COMS consists of two redundant systems; ene powered from Train A and the
   other from Train B. However, the two systems are not totally-independent,                              *
   in that an interlock exists between the two trains. The function of this
   interlock is to prohibit actuation of CCMS when RCS temperature is above
   350 degrees. The acceptability of this r.ondition needs to be reviewed by
   NRC-OSP Headquarters.
   Administrative Controls and Procedures
   The licensee has initiated several administrative controls which are
   intended to: (1) minimize the temperature differentials between the steam
   generators and reactor vessel while in a water-solid condition;
   (2) restrict the number of safety injection pumps to zero and centrifugal
   charging pumps to one when the RCS is in a low temperature condition; and
   (3) alert operators to the automatic operation of COMS. These administra-
   tive controls are contained in General Operating Instruction (GOI)-1,
   Plant Startup From Cold Shutdown To Hot Standby, rev. 61 and G0I-3, Plant
   Shutdown From Minimum Load To Cold Shutdown, rev. 33.
   Surveillance
                                                                                                          i
   As stated above, there are no TS surveillance requirements for COMS.
   However, because the RCS power operated relief valves (PORVs) and block
   valves are utilized for COMS, as well as utilized to alleviate high RCS
   pressure at power, these valves are addressed under TS surveillance
   requirements 4.4.3.2.1 and 4.4.3.2.2. These TSs require that the PORV be
   stroked every 18 months and the block valves every 92 days. Surveillance
   Instructions SI-166.40, Remote Valve Position Indication, and SI-166.1.1,                              ;
   rev. O, Full Stroking of Category "A" and "B" Valves Required in All
   Modes, implement these requirements.                  In addition, channel calibration and             ;
   operability verification of COMS has been accomplished using instrument
   maintenance instructions (IMI)-99 CC12.1, RCS Cold Overpressure Protection
   System Verification - Unit 1 and IMI-99 CC12.2, RCS Cold Overpressure
   Protection System Verification - Unit                    2.   In anticipation of the
   previously referenced to-be-issued TS, the licensee recently performed a
    review of these IMIs to assure their completeness and technical adequacy.
   This review revealed that these IMis were to be performed once every 18
   months during modes 4, 5, or 6, and testing of the final actuation devices
    (separation relays) was not required. As a result of these findings, the                              <
    licensee has revised the IMIs to include provisions for performance during
   modes 1, 2, and 3, and to include the testing of the final actuation
                                                                                                          '
   devices.    These revisions were accomplished with Instruction Change Forms
    87-2388 and 87-2389, and were approved on December 18, 1987. The
    inspector has reviewed the revised IMIs and determined that they
    adequately test the COMS. The inspector did, however, identify one area                               i
    in which these IMIs need further enhancement. The PORVs in COMS are                                   i
    target rock valves, similar in design and operation to those installed in                             !
    the Reactor Vessel Head Vent (RVHV) system. As noted in a previous                                    '
    inspection report (327,328/87-65), these target rock valves have exhibited
    the tendency to inadvertently open to 60% of full open when the block
    valves are opened at RCS system operating pressure, and then close within                              j
                                                                                                          l
                            ,.  - _ _ _ - . _ _ _ _ _                        _ _ _ , _ _ __ . . _ . _ - .
   .
                                        55
     about 5 seconds. The inspector noted that the above IMIs do not contain
     caution statements to alert the operator to the pcssibility of this
     occurrence.
    Observance of Branch Technical Position RSB 5-2
     The inspector's review of the Sequoyah COMS system also revealed the
     following items as they pertain to referenced paragraphs of Branch
     Technical Position RSB 5-2:
     -
           Paragraph B.3; COMS is a fully automatic system and is not manually
           enabled.  Therefore, an alarm to alert the operator to enable the
           system is not necessary.    Positive indication is not provided to
           indicate when the system is enabled. However, annunciation is
           provided to indicate when the protective action is initiated.
     -
           Paragraph B.4.a; Although the above referenced functional testing
           procedures now contain provisions to allow performance in modes 1, 2,
           and 3, there is currently no requirement for such testing to be
           performed prior to each shutdown.
     -
           Paragraph B.7; COMS does not depend on the availability of offsite
           power to function.    Train A is supplied from battery board I for
           Unit 1 and battery board III for Unit 2. Train B is supplied from
           battery board II for Unit 1 and battery board IV for Unit 2.
     As stated above, the NRC will review the adequacy of the system design as
     part of the TS approval process.

14. Review of Recent Management Changes

     The inspector reviewed certain recent management changes to determine
     whether they met appropriate requirements and commitments.       TS 6.3.1   ;
      states that, "Each member of the unit staff shall meet or exceed the
     minimum qualifications of ANSI N18.1-1971 for comparable positions and the
      supplemental requirements specified in Section A and C of Enclosure 1 of
      the March 28, 1980 NRC letter to all licensee's, except for the Site
      Radiological Control Superintendent who shall meet or exceed the
     qualifications of Regulatory Guide 1.8, September 1975."
                                                                                 I
      ANSI N18.1-1971 states that, at the time of initial core loading or
      appointment to the active position, the plant manager shall have ten years
      of responsible power plant experience, of which a minimum of three years
      shall be nuclear power plant experience. A maximum of four years of the
      remaining seven years of experience may be fulfilled by academic training  ,
      on a one-for-one time basis. To be acceptable, this academic training      :
      shall be in an engineering or scientific field generally associated with   l
      power production.   The plant manager shall have acquired the experience   )
      and training normally required for examinatica by tre NRC for a Senior     l
      Reactor Operator's License whether or not the examination is taken,
                                                                                 i
                                                                                 l
       -   ..             . -                -    --                      - ~ . .. .. .      .  ._ .   - .             - -
                                                                                                                                   r
                                                                                                                                   !
         *
              .
                                                                                                                                   >

'

                                                                                                                                   '
                                                                            56
                                                                                                                                   :
                                                                                                                                   b
                                                                                                                                   i
                In an organization which includes one or more persons who hre designated                                           l

l as principal alternates for the plant manager and who meet the nuclear l 1 power plant experience and NRC examination requirements established for  ! '

               the plant manager, the requirements of the plant manager may be reduced,-                                           r
                such that only one of his ten years of experience need to be nuclear power                                         ;
               plant experience and he need not be eligible for NRC examination.                                                   :

,

               At least one of the persons filling positions delineated in 4.2.1 should                                            i
                have a recognized baccalaureate or higher degree in an engineering or
                ~cientific field generally associated with power production,
                a.       The inspector reviewed the qualifications of the new plant manager
                         and determined that he has met the above above criteria . in the
                         following manner:
                         (1) He has over 21 years power plant expe_rience.
                         (2) All of the above experience was Nuclear Power Plant experience.
                         (3) This organization identi fie.s two individuals with signature                                         -
                               responsibility for the plant manager's office and could be
considered principal alternates with respect to the site -
 '
                               organization approved by the NRC in section 6 of the TS. One
                               individual, the operations supeHntendent, meets the following
l                              criteria:

.) I (a) He has approximately 20 years responsible power plant - ] experience.

                               (b) All of the above experience was . Nuclear Power Plant                                           '
                                      experience.                                                                                  ,

, ! (c) He received a PWR Licence Certification in 1982, based on  ! , the licensee's SR0 equivalency training for managers and .

 j                                    engineers.
                                                                                                                                   l

j (d) He holds a recognized baccalaureate degree in engineering. j (e) His training met the requirements specified in Section A  : i and C of Enclosure 1 of the March 28, 1980, NRC letter to f j all Licensees. < .

Considering the above, the inspector determined that the plant  !
                         manager's office currently meets TS 6.3.1.                                                                !

4.  : ) b. The inspector reviewed the qualifications of the new Assistant l l Manager of Nuclear power and determined that he has met the following  ;

'
                         criteria:                                                                                                  ,
                                                                                                                                   !

] (1) He has had over 15 years responsible power plant experience.  : 4 1 1 4

>

1

   , _         - _ _ . .                       _ _ _ _ _ _ _ _ _ . _ _ . _ - -          _ . , _      ,     . _ . - . , _ . _ . , _
           _       -_        ..        .    _         _ . . _      _    _    _ __             __
                                                                                                     __ -
                                                                                                           :
        *
          .                                                                                                j
                                                                                                           I
                                                              57

J

                                                                                                           t
                 (2) All of the above experience was Nuclear Power Plant experience.                       {
                 (3) He holds a recognized masters degree in Nuclear Engineering.

i This manager does not meet the requirements for examination for a I i Senior Reactor Operation License and has not completed the licensee's ,

SRO equivalency training for managers and engineers.  !
                                                                                                           '

! . l This position is not a line function and therefore is not covered .

                 under TS 6.3.1.           The inspector's review, . of this position, was                 i
                 completed to determine the depth of the qualifications of those                           !
                 persons acting as advisors to the site director only.                                     :

a i

                 ANSI N18.1-1971 states that. at the time of initial core loading or
  1. i
             c.
i                appointment to the active position, the maintenance manager shall-                        [
                 have a minimum of seven years of responsible power plant experience                       .

1

                 or applicable industrial experience, a minimum of one year of which                       l
                 shall be nuclear power plant experience. A maximum of two years of                        !
;
'
                 the remaining six years of power plant or industrial experience may                       l
                 be fulfilled by satisfactory completion of academic or related                           1
                 technical training on a one-for-one time. basis.                 He further should        !
                 have nondestructive testing familiarity, craft knowledge, and an                          !

! understanding of electrical, pressure vessel, and piping codes. l l c l The inspector reviewed the qualifications of the new Corporate [ j Maintenance Manager and determined that he has met the above criteria j

'
                 in the following manner:                                                                  ,
                                                                                                           i

i j (1) He has over 33 years of responsible power plant experience.  !

                                                                                                           I

1

                 (2) All of the above experience was power plant experience.                               '
                                                                                                           '
                 (3) He has the following additional qualifications:
!                      (a) Non-destructive testing familiarity,                                            i

I

                       (b) Craft knowledge.                                                                :

, l l (c) Understanding of electrical, pressure vessel, and piping I 3 codes.  ; l t i

              d. ANSI N18.1-1971 states that, "For those nuclear power plants having a                     i
                 manager designated to supervise the on ;ite professional - technical

i

                 groups, such managers, at the time of initial core loading or
                 appointment to the active position, should have a minimum of eight

' 2

                 years in responsible positions, of which one year shall be nuclear
                  power plant experience.                 A maximum of four years of the remaining

3

                  seven years of experience should be fulfilled by satisfactory
                  completion of academic training.                                                         ,

i

!
i
  .-. _   . .     .              _.     ..       . ..            .   -.   ._      -. - - - _ - - -
                                                                 .
                                                                                                              58
                                                                        The inspector reviewed the qualifications of the new Project Engineer
                                                                        and determined that he has met the above criteria in the following
                                                                        manner:
                                                                        (1) He has over 22 years in a responsible industry position.
                                                                        (2)            Eighteen years of the above experience was nuclear power plant
                                                                                       experience.
                                                                        (3) He holds a recognized baccalaureate and masters degree in
                                                                                       engineering.
                                                                        Considering the above, the inspector determined that the Project
                                                                        Engineer's qualifications currently meet TS 6.3.1.
                                                                   The inspector had no further questions. No violations or deviations were
                                                                   noted.
                                                             15.   Control Room Ventilation System
                                                                   The licensee through the performance of SI-144.2, Control Room Emergency           <
                                                                   Ventilation (CREV) Test, demonstrated the operability of the CREV three
                                                                   successive times for each train of CREV. The inspectors observed / reviewed
                                                                   each of these performances. In addition the following were reviewed:
                                                                         511-83, Rev. O, Control Building Emergency Pressure Ventilation Test
                                                                         CAQR SQP 87 1226
                                                                         OCN X000 91A, Damper 31A modification
                                                                         DCN X000 51A, Single failure modification
                                                                         DCN X000 119, Damper 31A-271 modification
                                                                         DCN X000 129, Mechanical equipment room related work

'

                                                                         Drawing 47W866 Series
                                                                   Issues still exist on the general control building flow balancing.
                                                                   However, these issues are not heatup or startup related and do not appear
                                                                   to affect the operability of the CREV. This issue is also discussed under
                                                                   LER 327/87-039. This issue is closed.

1

                                                                   (Closeo) LII 328/80-09-03; Main Control Room Habitability.
                                                                   Preoperational test (PT 333, R2 and PT 333, R3) indicated excessive in
                                                                   leakage to the Control Room (CR) during isolation conditions. Modifica-            l
                                                                   tions were accomplished to correct the identified deficiencies and                 l
                                                                   reported to NRC via reports dated April 3, 1980, December 15, 1980,                l
                                                                   January 30, 1981, and April 8,1982. Acceptable in-leakage was reported
                                                                   as achieved in the December 15, 1980 report. Additional modification was
                                                                   planned to further reduce air leakage to increase the margin of safety.
                                                                   The modification accomplished to reduce in-leakage installed blanks in the
                                                                   smoke removal fan ducts. Smoke removal will be accomplished by alternate
                                                                   methods (portable equipment).
 _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ - _ _ _ _ _ - _ _ _ _                 _ _ _ _ .
                                                                                  _
   .
                                         59
                                                                                    1
     This item is closed.

16. Followup on Operational Readiness Inspection Findings (IR 327,328/87--73)

     Prior to recommending the approval for Ser,uoyah Unit 2 heatup the items
     identified as open in IR 327,328/87-73 were resolved to the satisfaction
     of the NRC by TVA. These resolutions, in some cases completely closed the
     item and in some cases resolved the technical issues. The followup
     inspection and item status is provided below:
     a.    (Closed) URI 327,328/87-73-01; Problems associated with Containment
           Sump Level Transmitter. The issue identified involved the need to
           instruct the control room operators that the containment sump level
           transmitters had been re-evaluated and found to be operable and
           should be used in accordance with Emergency Operating Procedures.
           This was a change to the original plan which included changing
           procedures and training operators to not use these indicators for the
           first 6 hours following a loss of coolant accident (LOCA).        The    ,
           inspector verified that procedure IP-6 was revised and a letter was
           sent to each operator and to the training center to indicate that the
           original compensatory measure was no longer required.
     b.    (Closed) URI 327,328/87-73-02; The use of administrative controls to
           restrict cooling water inlet temperature to safety related coolers.
           This issue involved air flow problems associated with several safety-
           related room / space coolers with the auxiliary feed water (AFW) /
           boric acid transfer (BAT) pump area cooler being the most restric-
           tive.    Specifically, TVA had determined that in related equipment
           they would have to administratively control the ERCW inlet tempera-
           ture to the coolers to 72*F (most limiting) or take TS limiting
           conditions for operation (LCO) actions for equipment cooled by these
           coolers. This approach was discussed with OSP-HQ staff who agreed
           that the room / area coolers were attendant equipment for the controls
           could be used as long as TS actions were taken and documented on Form
           (ICF) 88-0057 to SI-3, "Daily, Weekly and Monthly Logs". When the
           ERCW inlet temperature reaches 72*F (most limiting), equipment served
           by the degraded coolers must be declared inoperable and the TS LCO
           action statement must be entered. It should be noted that history
           has shown that the Tennessee River will reach this temperature
           between May and October and a plant shutdown may be required if TVA
           cannot repair the degraded coolers.
                                                                                      l
     c.    (C1,osed) URI 327,328/87-73-03; Validation of Procedures Implementing
           Compensatory Measures; Operator Training and Use of Emergency Plan
           Implementing Procedures (IP) To Carry Out Compensatory Actions. A
           review of compensatory measures (cms) by TVA was made to identify
            implementing procedures which, due to the CM, required validation in      ,
           the form of a plant walk down of the procedure. Results of the             I
     -     validation are included below. As a result of this review, it was          I
           determined that the following procedures needed to be validated-         -
                                                                                      l
                                                                                      1
                                                                     __
  o .
                                      60
      *    IP-6; Activation and Operation of the Technical Support Center.
           It was determined that more detail was needed in the
           instructions for placing Lower Compartment Coolers in service in
           the event of the loss of a train of power. As a result of the
           procedure validation, a change was initiated to the procedure to
           include the specific valves which must be operated for loss of a
           given train of power.        A diagram was also added showing the
           location of these valves in the annulus.
           A01-8; Tornado Watch / Warning.      This procedure contained two
           checklists; one for verifying tornado doors closed and one for
           blocking doors open. Consequently, a the operator would have to
           jump back and forth between checklists and waste time in
           retracing steps. As a result of the validation, a procedure
           change was initiated to combine the two checklists into one
           checklist.     The doors on the checklist were arranged
           sequentially in such a manner that the operator could complete
           the checklist with minimal back tracking.      In addition, detailed
           locations of dampers were determined to be needed in the
           procedure. These were also included in the procedure revision.
      *
           A01-15; Loss of Component Cooling Water (CCS). A review of this
           procedure revealed that instructions for realigning spent fuel
           pit cooling from A train to B train CCS did not contain
            sufficient detail. A procedure enange was initiated to include
           the locations of valves requiring manual operation or local
           verification of position.
      The following changes to procedures were reviewed by the inspector
      and found to be acceptable:
                                                                                )
            IP-6, revision 19; Activation and Operation of Technical Support
            Center.    This revision implemented recommendations from the
            procedure validation walkdown as to operation of lower
            compartment coolers and the use of containment sump level
            transmitter and effects that environmental conditions may have
            on their accuracies.
                                                                                1
            A01-27,    revision 9; Control Rooms Inaccessibility.        This   l
            procedure change addressed the requirement to remove power fuses    ;
            to the main steam isolation bypass valves in the event of           l
            control room abandonment.
            A01-15, revision 9; Loss of Component Cooling Water.          This
            revision implemented recommendations from the procedure
            validation walkdown as to the aligning of "B" train CCS to spent

1 fuel pit heat exchangers upon loss of "A" train power.

       *
            A01-8, revision 16; Tornado Watch / Warning.       This revision
!           implemented recommendations from the procedure validation

! ,

 - - .       .   .        - - --
                 d
                                                                                                               '
                                                             61
                                                                                                               t
                                                                                                               .
                                    walkdown as to the operation of doors and dampers needed to
                                    protect the building during a tornado at the site.
                                                                                                               i
                         A followup review of operator training on the use of compensatory
                         measures and the need to follow radiological emergency plan
                                                                                                               '
                         implementing procedures (IP)- was conducted on January 19, 1988.
                         After the inspectors expressed their concerns with specific training                  !
                         of operators on compensatory measures the licensee conducted
                         augmented training which consisted of the following:
                         (1) Instructions were provided through a letter from the Operations
                                    Supervisor to all licensed operators dated January 18, 1988,
                                    regarding the use of IPs in general and the mandatory use of

3

                                    IP-6 for compensatory measures in specific.

l (2) Approximately 30-40 minutes of detailed training during shift

                                    turnover was provided to all of the 6 operating crews and                  ,
                                    commitments to review the need to include this training in
                                    operator requalification training was discussed with Plant
                                    management.
                                                                                                               O
                   d.    (Clostd) URI 328/87-73-04
                         (0 pen) URI 327/87-73-04; Need to Have 1 Additional ASE for Two Unit

4

                         Operation. This issue was discussed in IR 327,328/87-73 and was                       ,
                         addressed in the transmittal letter to that report. The purpose of
                         addrer. sing this issue in this report is to document that an
                         assess.nent for Unit 2 heat up was made by the NRC and the outstanding                i
                         issue did not impact the hold point release. decision.                                ,
                   e.    (0 pen) Violation 327,328/87-73-05; Failure to Perform Adequate 10 CFR

!

                         50.59 Safety Evaluations for Modifications to the Facility Which
                         Involved Compensatory Measures.
                         The TVA's safety evolutions (USQD) were developed and provided to the
                         NRC for their review prior to plant heatup.           The inspector's review

,

                          is provided below.          However, this item will remain open pending               '
                         issuance of the Notice of Violation and receipt of TVA's response.                     l

,

                         The inspector performed followup reviews of the unreviewed safety

1 question determinations (USQDs) as each pertains to the applicable ! compensatory measures (cms) listed below. Each was reviewed to  ;

                         determine the adequacy of the licensee's analysis of defeated                          i
                         automatic safety function.                                                             j
                                                                                                               :
                         (1) UNREVIEWED SAFETY QUESTION DETERMINATION, Identifier SQP871738 /                   l
SQT870649. This compensatory measure involved re-alignment of l

)

                                    ' ire pumps 2A-A and 2B-B to require manual start actuation by

j the operator. This action was necessary to prevent overloading

                                    of the Diesel Generator during a lov of coolant accident (LOCA)
                                    concurrent with a loss of offsite power     The assumption is that
                                    the containment temperatures will rise f.uf ficiently during the
                                     LOCA to activate the fire system and the additional electrical

i l

       . _ _   _
                      __         __      _    __                  _       _-            . _ _ _ _ _ _ _ , -__U

>

 .
                                   62
         load necessary to operate the fire pumps will overload diesel
         generators.
         The licensee determined that the CM provided for the defeated
         safety function will not degrade the auxiliary power system and
         the emergency core cooling system (ECCS) in the event of a LOCA
         concurrent with a loss of off-site power.       In addition, the CM
         will not defeat the fire protection when required. Technical
         Specifications were reviewed, sections pertaining to electrical
         power systems and fire suppression systems, and the USQD was
         found to be acceptable.
   (2) UNREVIEWED SAFETY QUESTION DETERMINATION, Identifier CAQR
         SQP871738RI / CAQR SQT870181IDI R0. A lack of adequate ground
         fault detection was identified on the 480V class 1E power
         system.    These circuits were tested once per shift. The test
         results have not been documented. A ^.M of testing the 480V IE
         power system has not been initiated to mandate the testing and
         to document the results. The USQD determined that no safety
         functions of the plant were being degraded, and no margin of
         safety as defined in the basis for any TS was reduced as a
         result of implementing the CM.      The inspector agrees with the
         licensee's assessment.
   (3) UNREVIEWED SAFETY QUESTION DETERMINATION, Identifier CAQR
         SQP871738 RI/ Memo A27830919018. To minimize the ingestion of
         hot gases or hydrogen into the air handling unit (AHU) ducts and
         to minimize heat addition in containment due to pyrolysis of
          foam insulation, a CM has been adopted to remove power from the
          ice condenser AHU followins a LOCA. The licensee has analyzed
         the issue and determined that removal of power to the ice
         condenser AHUs during a LOCA will not reduce any technical
          specification safety margin nor will it violate any requirements
         assumed in the safety analysis report (SAR).         The inspector
         determined that this USQD was acceptable.
   (4) UNREVIEWED SAFETY QUESTION DETERMINATION,           Identifier CAQR   ,
          SQP871738 RI/IDID-2.09.     The ERCW supply header to the station
          air compressors is a class H, non-seismic, line at the point
         where it enters the turbine building. A CM requiring the
          operator to isolate the breaker has been incorporated into A01-9    i
                                                                             '
         which is more explicit then the previous requirement contained
          in 501-55-0M-278-XA-278-D.      The licensee has evaluated this
          issue and determined that the consequences of an accident are
          not increased by the revised procedure.         In addition, the
          licensee has committed to correct the deficiency and therefore
          eliminate the US00 by adding automatic isolation of the ERCW
          flow that would result from a non-seism'c line break.         This
          commitment is to be incorporated prior to          U-2, mode #2
                                                                              '
          operation. The licensee currently is tracking this modification
                                                                             I
                                                                             I
   -     .- -        -          .    . _  - _ -        -       - ~ -                  . _ _       - .
                                                                                                      ,
     .
                                                                                                      i
       .
                                                                                                      ;
                                                                                                      <
63 l

1

                                                                                                      '
                    on the restart P-2 schedule. However, the USQD determined that
                    the CM was acceptable for plant operations.                                       -

4

(5) UNREVIEWED SAFETY QUESTION DETERMINATION, Identifier CAQR j
                    SQP871738/ECHLO73. Weight indicating system for the upper head
 '
                                                                                                      l
                    injection does not function .and the annunciators have been                       !
                    disabled.      This item is a mode 3 issue and the licensee                       ,
                    currently has a mode 3 RTI 1.1 punchlist item to ensure it u                      ;
                    completed prior to mode 3.           The inspector will review the USQD           !
                    and CM prior to mode 3.                                                           -
              (6) UNREVIEWED SAFETY QUESTION DETERMINATION,                  Identifier CAQR          l
                    SQP871738      RI/CAQR      SQP87183   R0.       Containment   electrical         i
                    penetration conductors do not have circuit protection as                          .
                    required by design criteria, SQN-DE-V-11.3.                Failure of this        !
                                                                                                      ~

( electrical equipment could potentially violate containment

                     integrity. However, these are not to be used in modes 1, 2, 3,                   l
                    and 4 without adaing the circuit protection. The licensee has                     l
                    evaluated the issue and determined that testing using these                       i
                    penetrations can only be performed in modes 5 and 6.                      In      i
                    addition, the test connections are to be de-energized prior to
                    entering mode 4. The inspector agreed with the licensee

a

                     assessment provided by the USQD.                                                 ,

I (7) UNREVIEWED SAFETY QUESTION DETERMINATION, 'dentifier CAQR j

t                    SQP871738 RI/ Memo S53851206915. Limits on radiation levels in

1

                     the evaporator bottoms going to the boric acid tanks.                  (BAT)
                                                                                                      '

l have been established to ensure that the area around the boric i i acid tanks could be classified as a mild environment. A CM has

                     been initiated to check for Cs-137 to verify that the liquid is                   1

3

                    within acceptable activity level prior to transferring to the                      j

4 BAT. '

i                                                                                                      l

i' The licensee determined that the CM has no effect on the basis

                       for any TS and therefore the margin of safety is not reduced.
                     This USQD was found to be acceptable.

I (8) UNREVIEWED SAFETY QUESTION DETERMINATION, Identifier CAQR SQP

                     871738 RI/EC 230.01. The ability of Ruskin fire dampers to                        i
                      close against normal operating flow have been questioned,                        i

1 Ruskin filed a 10 CFR, Part 21 with the NRC on this condition.

                      The licensee evaluated the condition and ten fire dampers were
                       identified which require compensatory measures in order to
                       perform their safety function.         The inspector questioned the              ,
                       licensee on the time needed to perform these actions and after
                                                                                                       '
                       several discussions was satisfied that the USQD adequately
                       addressed the CH.
               (9) UNREVIEWED SAFETY QUESTION DETERMINATION, Identifier CAQR
                       SQP871738 / SCRSQNMER8677, The spent fuel pool (SFP) heat
                       exchangers must be realigned to train 'B' component cooling                     i
                                                                                                       !
                                                                                                       l
                                                                                                       l
                                                                                                      j
   .     _ -       _ -   -- .               .-      --
                                                           - . - . _ . - ..            -.                     ..             .
                                                                                                                                          T
                                                                                                                                          ;
                 -
                       .                                                                                                                  :
                                                                                                                                          ?

j 64 l

                                         system (CCS) upon the loss of train 'A' power. This requires                                     ;
                                         operator action to manually operate certain CCS valves through a                                 i
                                         mechanical action.                                                                               !
                                         The licensee evaluated this condition and determined that no
                                         margin of safety as defined in the TS has been reduced by the
                                         implementation of the CM.            This USQD was found to be acceptable.

l (10) UNREVIEWED SAFETY _ QUESTION DETERMINATION, Identifier CAQR <

                                         SQP871738RI / CAQR SQP871477 IDI R0.             The flex hoses installed                        i
                                         to connect the diesel generator heat exchangers to the essential                                 t

] raw cooling water (ERCW) supply have not been qualified to  ;

                                         withstand a seismic event. A CM has been implemented requiring                                   '

i operator action to visually inspect the flex hoses prior to ! '

                                         Unit 2 restart and after each diesel generator start.                        This                .
                                         action was recommended by the licensee's consultant who
                                         evaluated the capability of these hoses to withstand a SSE event                                 .
                                                                                                                                          '
                                         although.they were not purchased to seismic specifications.
                                                                                                                                          r
                                         The licensee has evaluated this condition and determined that no                                 j
                                         plant safety function or operation will be adversely affected or
                                         degraded by the visual inspection and that no possibility for an
                                         accident or malfunccion of a dif'erent type than any evaluated                                   1

,

                                         previously in the safety analysis report is created by the                                       .
implementation of the CM. 1

~

                                                                                                                                          i

! (11) UNREVIEWED SAFETY QUESTION DETERMINATION, Identifier CAQR *

                                         SQP871738 R1/CAQR SQF870022 R0.              Manual opening of various                           :
                                         auxiliary building interior doors are required upon a tornado                                    !

.

                                         alert. The impact of opening these doors when a tornado warning

1

                                          is in effect was evaluated by the licensee. This evaluation                                     :

I

                                         considered fire protection, toxic gas control, electrical                                        I

, '

                                          separation / isolation,           physical  security,              environmental                l
                                         qualification, external missile protection, procedural error,                                    i

<

                                         and radiation hazards. Based on the required fire watches                                        !
                                         associated with opening the doors, the licensee has determined
                                         that no reduction of safety margin as defined in the basis for
                                         any technical specification has occurred. Additionally, the

! licensee modified the procedures to start compensatory actions

                                         on a tornado watch,                                                                                i

1 l l (12) UNREVIEWED SAFETY QUESTION DETERMINATION, Identifier CAQR l

                                          SQP871738 RI/IDID-22-7. A requirement for operator action to
'
                                                                                                                                            '
'
 i                                        turn off the ERCW ventilation fans when pumping station
                                          temperature reaches 65 F or less has been implemented as a CM.

1 This requirement was implemented to prevent freezing of portions

t
                                          of the ERCW system during the winter months.

j

                                          The licensee has evaluated this CM and determined that the plant
                                          margin of safety has not been reduced by this CM and the changes

'

                                                                                                                                           >

a

 .
                                                                                                                                          i
                                                                                                                                          '

4 d

     -__     __.         _ _ - _ _               ,._ - __                 ,                     _ __ _ _ __. __     -
                                                                                                                        _._.___._,_..__,.J
                                                       *
                                                         O
                                                                                           65
                                                                  does not introduce any events not previously analyzed in the
                                                                  FSAR.
                                                           (13) UNREVIEWED SAFETY QUESTION DETERMINATION,          Identifier CAQR
                                                                  SQP871738 RI/CAQR SQP870217 R0. Valves on the ERCW header that
                                                                  supply cooling water to the condensers on the air conditioning
                                                                  systems to the (1) main control room, (2) electrical board room
                                                                  and, (3) shutdown board room do not function as designed. This
                                                                  condition prevents proper ERCW flow to these condensers.        The
                                                                  standby trains will not automatically start when the respective
                                                                  normal train fails. The CM is for the operator to manually
                                                                  start the standby train and to manually open/ throttle the ERCW
                                                                  flows to the subject air conditioning condensers.
                                                                  The licensee has evaluated this condition and determined that no
                                                                  plant safety function will be adversely affected by the
                                                                  implemen'* tion of the subject CM,
                                                           (14) UNREVIEWED SAFETY QUESTION DETERMINATION,          Identifier CAQR
                                                                  SQP871738 RI/NRC 6.22, Physical separation of auxiliary control
                                                                  air system air headers inside containment to prevent adverse
                                                                  interactions have been previously identified. In addition, the
                                                                  control building air handling system logic switching
                                                                  configuration appears to be inadequate (i.e., once the control
                                                                  logic switches from an operating train which has lost auxiliary
                                                                  control air to a standby train, the control logic will not
                                                                  switch back to the original train if it regains auxiliary
                                                                  control air and the second train fails).        Required operator
                                                                  actions have been implemented to perform the necessary changes.
                                                                  A line break would be followed by a header isolation signal.
                                                                  However, a temporary loss of air supply would cause a temporary
                                                                  failure and auto transfer to the backup unit.
                                                                  The licensee has evaluated this condition and determined that
                                                                  the ability of this equipment to perform its intended function
                                                                  has not been affected adversely by the implementation of the CM
                                                                  and no new malfunctions of accidents, are foreseen.        Therefore
                                                                  no margin of safety reduction would result.
                                                            (15) UNREVIEWED SAFETY QUESTION DETERMINATION, Identifier SQP871738RI
                                                                  /SCRSQNNEB8617.    Manual operation of valve HCV-77-920, is
                                                                  required to prevent flooding of the annulus due tu a moderate
                                                                  energy line break. This action is to be performed within 15
                                                                  minutes of a high level alarm in the annulus drain sump in order
                                                                   to drain the annulus to the auxiliary building sump. Operating
                                                                   instructions have been developed to provide surveillance of the
                                                                   annulus drain sump alarm system and provisions have also been
                                                                  developed for inspection of the annulus for flooding if the
                                                                   alarm system is inoperable.       A review of the applicable
                                                                  maintenance "Detailed Work Instruction," PM 2135-040, rev. O,

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

                                                                       -- .        . _ -      - . -          .         .             .
                                                                                                                                        :
                                                                                                                                        ?
                                                                                                                                        :
              .
                                                                                                                                        l
                                                                                                                                        t
                                                                    66

i ,

                                         revealed that a requirement for posting a watch existed if                                     f
                                         either of the annulus sump level switches are inoperable. An                                   [
                                         evaluation by the licensee had determined that the                                             !
                                         implementation of the CM will not result in a lesser margin of.                                !
                                         safety than that-analyzed.                                                                     ,

i (16)UNREVIEWED SAFETY QUESTION DETERMINATION, Identifier CAQR "

                                         SQP870031 / SQN SQA 119. A problem associated with the                                         <
unreliability of ERCW supply valves providing cooling water to
the emergency diesel generators has been identified. CM i

1 requiring an operator to provide assurance that these valves l

                                         open on demand has been initiated for instances when the valves                               1
                                         have been overtightened or handtightened. However, the operator
                                         for these valves are to be replaced prior to restart which will                                !

, eliminate the need for this CM.  ;

                                                                                                                                        t

!. The licensee has evaluated the condition and determined that i with the operations limitations and actions specified, no j

                                                                                                                                        ~
                                         failure of the Diesel Generators, due to a failure of the ERCW
                                         supply valves to operate, is foreseen.          However, these                                 i

4

                                         limitations and actions may be cancelled when the Rotork                                       :

4

                                         operators are replaced. The licensee has further stated that                                   i

3

                                         when these actions are completed, prior to mode #2, full
                                         reliability of the diesels are assured and the plant can be                                    i
operated without impact on safety. l
                                                                                                                                        ;
                                                                                                                                         I
                  17.         Containment Walkdown
                                                                                                                                        ;

! On January 19, 1988, two NRC inspectors accompanied TVA manLgement on a j tour of the Unit 2 containment. The purpose of this containment tour was j to evaluate plant material condition within the containment prior to plant i i heatup. The items identified by the inspector were discussed with TVA for  ; I correction. The items included the following: 1 ! a. Penetration X79B cap bolts did not have proper thread engagement. ! b. Crane stop on manipulator crane is missing. !

i                             c.    Limit switch for air return fan damper on elevation 734 inside hatch
                                   does not contact actuator arm.

l d. RHR containment sump screen is frayed and needs to be secured. }

                              e.    RHR containment sump ground strap is disconnected,
                              f.    Temperature element 2-TE-68-386 or TE-1324 is not properly secured.
                              g.    Lower containment drain inside polar crane wall near PRT is stopped                                   l

l up.  ! l l

                                                                                                                                          l

4

  --y. c_ . .   _.-,n.,,m,m,,                , . , _ , .
                                                           ..____ _                                 _
                                                                                                      v-,,,-   , , .._   .,-c.,- ,-1
   _ . _.         _ _ _ . -__            _    _ - . __        _ .      .                _.            _

d 1

      .

.

                                                          67                                                 !
                                                                                                             -
i

! h. Excore basket positioning devices need to have locking pins installed  ; 4

                         on upper and lower rods.

l 1. Reactor coolant SG/RCP cross-ander piping on loop 1 has loose cable * l tension and the whip restraining device is cocked and has t been L j rubbing it's stop.

 i
              J.         Air return fan flow devicis have nylon tubing installed.           Is_this          I
                          installation permanent and will it be needed during a LOCA?
              k.         Air lock doors need gasket cleaned, inspected, and lubricated as
                         necessary.
              1.         All steam generator manway cover lif ting tools are not secured. Is
                         this a problem?                                                                     ,
              m.         2-PI-68-42 RCS loop 3 hot leg sample pressure gauge needs face glass-
                          replaced.                                                                          '
              The licensee also identified several' items that needed correction. The
              licensee initiated action to evaluate and correct the above items along                         l
              with items they identified.              Items a.    -
                                                                     e., h., k. ,1. , and m. were
              corrected with work requests (WR). Item f. was determined to be asso-

1 ciated with the RVLIS system and a WR was issued to correct the problem.

 '
              Iten i. was corrected with a WR however, the licensee was requested to
 >
              evaluate thermal movement of loop 1 cross-under piping during thermal
              expansion testing STI-62. Item g. was reported corrected by the cleanup
              crew.           Item j. was corrected by field change request (FCR) 6698 which

i removed the tubing and blanked the lines. The instruments which were

              supplied by these instruments were determined to be non-safety and are not
              used to operate the equipment during accident conditions. Additionally,
 1            the instruments in the control room were marked as not operational. Item
              m. was evaluated by licensee as not requiring to be restrained and an
              engineering evaluation was performed to support this decision.

]

          18. IE Bulletins (92071)
              IE Bulletins (IEBs) are documents issued by the NRC which require certain
              specific actions of the addressee. The inspector has reviewed the actions

j taken by the licensee as a response to the below listed IEBs. The

i
               inspector verified that corrective actions appeared appropriate; gent..*ic
              applicability had been considered; the licensee had reviewed the event and
              that appropriate plant personnel were knowledgeable; no unreviewed safety

4

              questions were involved; and that violations of regulations or Technical
              Specification conditions did not appear to occur.
              (0 pen) IEB 87-02; Fastener Testing To Determine Conformance with
              Applicable Material Specifications.                 The inspector participated with             ,
y              licensee materials engineers in selecting the 40 fastener samples required                     I
               to be tested per action paragraph two (2) of the bulletin and TI 2500/26.

'

                                                                                                              1
                                                                                                              l
)                                                                                                             !
                                                                                                              l
                                                                               __--__-__________--___-_____-A

,

 * .
                                        68
    Twenty samples were selected from safety-related and twenty samples from
    non-safety related. The samples were further broken down into ten from
     studs, bolts, and/or capscrews and ten from nuts for both the safety
     related and the non-safety related categories.          The sample included
     fasteners from the categories of the bulletin including some from SAE
    grade J429 with markings RT, H, and KS. The samples were tagged and
    bagged for shipment to the test lab. The data sheet for each item denoted
     the fastener description, location, contract item, material specification,-
     head markings and QA level. The data sheet was stapled to the bag
     containing the sample. This information will allow TVA to identify any
     application that the parts being tested are used for. The following is a
     list of material selected:
                            SAFETY RELATED BOLTS / STUDS
           Material                              Siz,e
           A193, B7                        .5 x 13 UNC x 5
           A193, B7                        9/16 x-12 UNC x 4
           A193, B7                        .5 x 12 UNC x 4
           316                             .875 x 9 UNC x 6
           A193, B8M                       .5 x 13 UNC x 4
           A449                            1/4 x 20 UNC x 3
           A307, GR B                      1.375 x 6 UNC x 6
           A307, FR A                      .562 x 12 UNC x 4
           304                             .412 x 18 UNC x 1.5
                                SAFETY RELATED NUTS
                 Material                              Size
                 A194, 2H                        .5 x 13 UNC
                 A194, 2H                        3/4 x 10 UNC
                 A563, A                         .625 x 11 UNC
                 A194, 8M                        .312 x 18 UNC
                 SA194, 8M                       .562 x 12 UNC
                 A563, B                         .25 x 20 UNC
                 SAE J995, 8                      .875 x 9 UNC
                 A194, 7                         1.75 x 8 UNC
                 A194, 2H                        I x 8 UNC
                 316                              .875 x 9 UNC
                              NON-SAFETY BOLTS / STUDS
                 Material                               Size
                 A193, B7                        3/4 x 10 UNC x 5
                 SAE J429, 5                      1/4 x 28 UNF x 2 1/2
r
  -
        .
                                              69
                    SAE J429, 8                      7/8 x 9 UNC x 3 1/2
                    SAE J429, 8                      3/8 x 16 UNC x 1.5
                    SAE J429, 8                      1/2 x 13 UNC x 3.5
                    SAE J429, 8                      3/4 x 10 UNC x 2
                    SAE J429, 8                      3/8 x 10 UNC x 3.5
                    18-8                             1/2 x 13 UNC x 1 3/4
                    18-8                             3/8 x 16 UNC x 1.5
                    A193, B8                         1/4 x 20 UNC x 1.25
                                        NON-SAFETY NUTS
                    Material                         Size
                    CS                                .25 x 28 UNF
                    SS                               .25 x 20 UNF
                    A563, A                          1.5 x 6 UNC                        ;
                    Steel                            1.75 x 5 UNC
                    J995, 8                           .164 x 32 UNC 5 samples
                    CS                                .875 x 9 UNC
                    CS                                .19 x 24 UNC
                    SS                                .625 x 11 UNC
                                                                                        !
    19.   List of Abbreviations Unit I and 2                                            '
          AI        -
                          Administrative Instruction
          AFW       -
                          Auxiliary Feedwater
          AVO       -
                          Auxiliary Unit Operator
          A01       -
                          Abnormal Operating Instruction
          ASME      -
                          American Society of Mechanical Engineers
          BIT       -
                          Boron Injection Tank
          C&A       -
                          Control and Auxiliary Buildings
          CAQR      -
                          Conditions Adverse to Quality Report

. CCP -

                          Centrifugal Charging Pump
CCS -
                          Component Cooling System
i
          CCTS      -
                          Corporate Commitment Tracking System

I COPS -

                          Cold Overpressure Protection System
l         CS        -
                          Containment Spray                                              ;

) CSSC -

                          Critical Systems and Components
          CST       -
                          Condensate Storage Tank
          DBVP      -
                          Design Baseline Verification Program                           ,
          DC        -
                          Direct Current                                                 '
          DCN       -
                          Design Change Notice
          DNE        -
                          Division of Nuclear Engineering                                ,
          ECCS       -
                          Emergency Core Cooling System                                  ,
          ECN        -
                          Engineering Change Notice                                      l
          EDG        -
                          Emergency Diesel Generator
                                                                                        ]
          EGTS       -
                          Emergency Gas Treatment System                                 l
          EMI        -
                          Electric Magnetic Interference                                 i
i         EQ         -
                          Environmental Qualification
ERCW -
                          Essential hav Cooling Water

( l 1 1 .

                                                                                         l
                                                                    _.,.--..m-. _ , , -
                                                              }
                                                               ,
 ,
  • .
                                    70
                                                              i
     ESF    -
                Engineered Safety Feature
     FCR    -
                Field Change Request                          .
     FSAR   -
                Final Safety Analysis Report                  '
     H0     -
                Hold Order
     HP     -
                Health Physics
     HQ     -
                Headquarters
     HVAC   -
                Heating, Ventilation, and Air Conditioning
     IDI    -
                Integrated Design Inspection
     IE     -
                Inspection and Enforcement
     IEB    -
                Inspection and Enforcement Bulletin
     IFI    -
                Inspector Followup Item
     IMI    -
                Instrument Maintenance Instruction
            -
     KV         Kilovolt
     LER    -
                Licensee Event Report                         '
     LCO    -
                Limiting Condition for Operation
     LOCA   -
                Loss of Coolant Accident
     MI     -
                Maintenance Instruction
     MOVATS -
                Motor Operated Valve Testing
     MSIV   -
                Main Steam Isolation Valve
     NEP    -
                Nuclear Engineering Procedures
     NRC    -
                Nuclear Regulatory Commission
     ODCM   -
                Offsite Dose Calculation Model
     OSP    -
                Office of Special Projects
     PD      -
                Positive Displacement
     PI      -
                Pressure Instrument
     PM      -
                Preventive Maintenance
     PMT     -
                Post Modification Test
     PORV    -
                Power Operated Relief Valve
     PORS    -
                Plant Operation Review Staff
     PRO     -
                Potentially Reportable Occurrence
     QA      -
                Quality Assurance
     QC      -
                Quality control
     RARC    -
                Radiological Assessment Review Committee
     RCS
             -
                Reactor Coolant System
     RCP     -
                Reactor Coolant Pump
     RHR     -
                Residual Heat Removal
     R0      -
                Reactor Operator
     RTD     -
                Resistance Thermal Devices
     RTI     -
                Restart Test Instruction
     RWP     -
                Radiation Work Permit
      RWST   -
                Reactor Water Storage Tank
     SER     -
                Safety Evaluation Report
      SFP    -
                Spent Fuel Pool
      SG     -
                Steam Generator
      SI     -
                 Surveillance Instruction
      SIS    -
                 Safety Injection System
      SMI     -
                 Special Maintenance Instruction
      501     -
                 System Operating Instructions
      SR0     -
                 Senior Reactor Operator
      550MI   -
                 Safety System Outage Modification Inspection

(

 o . 'o
                                   71
        STI   -
                Special Test Instruction
        TACF  -
                Temporary Alteration Control Room
        TAVE  -
                Average Reactor Coolant Temperature
        T0AFP - Turbine Driven Auxiliary Feedwater Pump
        TS    -
                Technical Specificati3et
        TSC   -
                Technical Support Cen'.er
        TVA   -
                Tennessee Valley Authority
        UHI   -
                Upper Head Injection
        URI   -
                Unresolved Item
        USQD  -
                Unresolved Safety Question Determination
        VCT   -
                Volume Control Tank
        VIO   -
                Violation
        WCC   -
                Work Control Center
        WP    -
                Work Plan
        WR    -
                Work Request
                                                         i
                                                          l
                                                          !
                                                          l

}}