ML17264A551

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Monthly Operating Rept for June 1996 for Ginna Station. W/960711 Ltr
ML17264A551
Person / Time
Site: Ginna Constellation icon.png
Issue date: 06/30/1996
From: WALDEN J D, WIDAY J A
ROCHESTER GAS & ELECTRIC CORP.
To: VISSING G S
NRC (Affiliation Not Assigned), NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9607170017
Download: ML17264A551 (9)


Text

/DISTRIBUTION CODE:IE24DCOPIESRECEIVED:LTR ENCLSIZE:TITLE:Monthly,Operating Report(perTechSpecs)NOTES:License Expdateinaccordance with10CFR2,2.109(9/19/72).

05000244CATEGORYj.REGULATOR INFORMATION DISTRIBUTION STEM(RIDS)ACCESSION NBR".9607170017 DOC.DATE:

96/06/30NOTARIZED:

NO'DOCKETFACIL:50-244 RobertEmmetGinnaNuclear.Plant,Unit1,Rochester G05000244AUTH.NAMEAUTHORAFFILIATION WALDEN,J.D.

Rochester Gas6ElectricCorp.WIDAY,;G.A.

Rochester Gas6ElectricCorp.RECI(,.NAME RECIPIENT AFFILIATION VZSSINh,G.S.

DocumentControlBranch(Document ControlDesk)

SUBJECT:

Monthlyoperating reptforJune1996forGinnaStation.W960711ltr.RECIPIENT IDCODE/NAME PD1-1PDhCOPIESLTTRENCL11RECIPIENT IDCODE/NAME G..COPIESLTTRENCL11INTERNAL:

AEOD/SPD/RRAB NRR/DRPM/PECB EXTERNAL:

LITCOBRYCE,JHNRCPDR11111111RGN1NOACTR0111111~D0ENNOTETOALL"RZDS"RECIPIENTS:

PLEASEHELPUSTOREDUCEWASTE!CONTACTTHEDOCUMENTCONTROLDESK,ROOMOWFN5D-5(EXT.

415-2083)

TOELIMINATE YOURNAMEFROMDISTRIBUTION LISTSFORDOCUMENTS YOUDON'TNEED!'TOTALNUMBEROFCOPIESREQUIRED:

LTTR9ENCL9 ROCHESTER GASANDELECTRICCORPORATION o89EASTAVENUE,ROCHESTER, N.Y.14649.0001 TELEPHONE AREACODC7>a546-2700July11,1996USNuclearRegulatory Commission DocumentControlDeskAttn:GuyS.VissingProjectDirectorate I-1Washington, DC20555

Subject:

MonthlyReportforJune,1996Operating StatusInformation R.E.GinnaNuclearPowerPlantDocketNo.50-244

DearMr.Vissing:

PursuanttoGinnaImprovedTechnical Specifications Section5.6.4,attachedisthemonthlyoperating statusreportforGinnaStationforthemonthofJune,1996.Verytrulyyours,+JosephA.WidayPlantManagerxc:U.S.NuclearRegulatory Commission Mr.GuyS.Vissing(MailStop14C7)ProjectDirectorate I-1Washington, D.C.20555/U.S.NuclearRegulatory Commission RegionI475Allendale RoadKingofPrussia,PA19406U.S.NuclearRegulatory Commission Mr.W.H.LovelaceMNBB7602Washington, D.C.20555U.S.NRCGinnaSeniorResidentInspector Attachments 9607170017 960630PORE""ADOGK05000244iR,tl~,gp(~PDRL, r~cCOMPLETED BY:Jul11199650-244JohnV.WaldenTELEPHOE(716)771-3588Notes1.UnitName:R.E.GINNANUCLEARPOWERPLANT2.Reporting Period:June19963.LicensedThermalPower(MWt):15204.Nameplate Rating(GrossMWe):5175.DesignElectricRating(NetMWe):4706.MaximumDependable Capacity(GrossMWe):4907.MaximumDependable Capacity(NetMWe):4708.IfChangesOccurinCapacityRating(ItemsNumber3Through7)SinceLastReport,GiveReason:9.PowerLeveltoWhichRestricted, IfAny(NetMWe:10.ReasonForRestrictions, IfAn:ThisMonthYr.-toDateCumulative-11.HoursinReportedPeriod12.NumberofhoursReactorWasCritical13.ReactorReserveShutdownHours14.HoursGenerator On.line15.UnitReserveShutdownHours16.GrossThermalEnergyGenerated (MWH)17.GrossElectrical EnergyGenerated (MWH)18.NetElectrical EnergyGenerated (MWH)19.UnitServiceFactor(%)20.UnitAvailability Factor(%)21.UnitCapacityFactor(usingMDCNet)(%)22.UnitCapacityFactor(usingDERNet)(%)23.UnitForcedOutageRate(%)720.0503.30.0462.60.0631374.0214132.0203264.064.264.260.160.10.04367.02612.60.02568.60.03704308.0 1259724.0 1197305.0 58.858.858.358.33.2233135.0186279.61687.6'83317.38.5'60567616.0 86322224.0 81945117.0 78.678.675.875.85.524.Shutdovms Scheduled OverNext6Months(Type, DateandDurationofEach):25.IfShutdownAtEndofReportPeriod,EstimateDateofStartup:26.UnitsinTestStatus(PriortoCommercial Operation):

Foresst,Achieved INITIALCRITICALITY INITIALELECTRICITY COMMERCIAL OPERATION

'UMULATIVE TOTALCOMMENCING JANUARY1,1975'*CUMULATIVE TOTALCOMMENCING NOVEMBER8,1969

'eCy'll$

AVERAGEDAILYUNITPOWERLEVELDOCKETNO:50-244UNIT:R.E.GinnaNuclearPowerPlantDATE:Jul111996COMPLETED BY:JohnWaldenTELEPHONE:

716771-3588MONTHJune1996DAYAVERAGEDAILYPOWERLEVEL(MWe-Net)

DAYAVERAGEDAILYPOWERLEVEL(MWe-Net) 17.4872.18.4913.19.49420.46521.4726.22.7~-1323.4948.-1424.4949.-1525.49310.4726.49016027.48812.28.48913.11229.49114.35630.48715.45531.16.488INSTRUCTIONS Onthisformat,listtheaveragedailyunitpowerlevelinMWe-Netforeachdayinreporting month.Computetothenearestwholemegawatt.

lAI4,<gvqg DO(KETNOSO-244UNITNAhlE RE.GINNANUCLEARUNITSHUTDOWNANDPOWERREDUCTIONS DATI:.COhtPLI'.l'I'.D BY~'hnV.WaldenqI:.LI:.PIIO:

716771-3588foWER,PLANT I>~No.Date0QC0oQLOl~0cu0o0l/lC0ClLicenseeEventReporthEw0EACOIllCQooOCauseLCorrective ActiontoPreventRecurrence 4/1/96S226.0CScheduled shutdownforrefueling andmaintenance.

6/10/96Blowdownsystemwasoperatedimproperly whichallowedairto.enterthecondenser.

Highturbinebackpressureresultedinaturbinetripwiththereactorremaining critical.

6/12/96S29.6BScheduled shutdownforturbinetestingandrepairs,ofsecondary systemleaks.6/20/96F12.7APowerreduction forrepairsofoff-sitecircuit908.Turbineremainedon-line.1F:ForcedS:Scheduled REV.4/85494t9Reason:A-Etluipmcnt Failure(Explain)

B-Maintenance orTestC-Refueling D-Regulatory Restriction E-Operator Training&LicenseExamination F-Administrative G-Operational Error(Explain)

H-Other(Explain) hlethod:I-hfanual 2-ManualScram.3-Automatic Scram.4-Other(Explain)

ExhibitG-Instructions forPrcparatton ofDataEntrySheetsforLicenseeEventReport(LER)File(NUREG-0161)ExhibitI-SameSource E'p(,

NARRATIVE SUM5GWYOFOPERATING EXPERIENCE DOCKETNO:50-244UNIT:R.E.GinnaNuclearPowerPlantDATE:Jul111996COMPLETED BY:TELEPHONE:

JohnWalden716771-3588MONTHJune1996Theunitwasstartedupandbroughton-lineonJune10,1996.AturbinetripoccurredonJune10,1996duetohighturbinebackpressure.

Theunitwasplacedbackon-lineonJune10,1996.Ascheduleunitshutdownforturbinetestingandsecondary systemmaintenance tookplaceonJune12,1996.Theunitwasplacedone-lineonJune13,1996.Powerascension waslimitedbyfuelconditioning.

FullpowerwasreachedonJune15,1996.Apowerreduction occurredonJune20,1996duetoafailureontheelectrical distribution systemoffsite.Theunitwasreducedto72'.powerwhilerepairsweremade.Theunitremainedatfullpowerfortheremainder ofthemonth.